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Category:CORRESPONDENCE-LETTERS
MONTHYEARSVP-99-181, Forwards Biennial Update to Quad Cities Ufsar,Iaw 10CFR50.71(e).Update Includes Changes to Facility & Procedures & Are Current Through 9906301999-10-20020 October 1999 Forwards Biennial Update to Quad Cities Ufsar,Iaw 10CFR50.71(e).Update Includes Changes to Facility & Procedures & Are Current Through 990630 ML20217H4661999-10-18018 October 1999 Forwards Changes to EPIPs IAW 10CFR50.54(q) & 10CFR50,App E, Section V.Details of Changes Encl ML20217K7011999-10-13013 October 1999 Provides Response to Questions Related to Request for License Amend,Per 10CFR50.90, Credit for Containment Overpressure. Supporting Calculations Encl 05000254/LER-1999-004, Forwards LER 99-004-00,IAW Requirements of 10CFR50.73(a)(2)(i)(B).Util Is Committed to Listed Action1999-10-12012 October 1999 Forwards LER 99-004-00,IAW Requirements of 10CFR50.73(a)(2)(i)(B).Util Is Committed to Listed Action ML20217F6321999-10-0707 October 1999 Forwards Insp Repts 50-254/99-01 & 50-265/99-01 on 990721- 0908.No Violations 05000254/LER-1999-003, Forwards LER 99-003-00 IAW 10CFR73(a)(2)(v)(A).Commitment Made by Util,Listed.Any Other Actions Described in LER Represent Intended or Planned Actions by Licensee1999-10-0707 October 1999 Forwards LER 99-003-00 IAW 10CFR73(a)(2)(v)(A).Commitment Made by Util,Listed.Any Other Actions Described in LER Represent Intended or Planned Actions by Licensee ML20212K9421999-10-0505 October 1999 Informs That NRC Accepts 990513 Inservice Inspection Relief Request CR-31 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20216J8241999-09-30030 September 1999 Notifies of Removal of NRC Headquarters & Region III Offices from Controlled Copy Distribution of Certain CE Documents. Specific Documents,Associated Controlled Copy Numbers & NRC Location Affected Are Shown on Attachment to Ltr SVP-99-189, Confirms Completion of Actions Identified During Review of NRC Safety Evaluation of Boiling Water Reactor Owners Group Rept, Utility Resolution Guidance of ECCS Suction Strainer Blockage1999-09-22022 September 1999 Confirms Completion of Actions Identified During Review of NRC Safety Evaluation of Boiling Water Reactor Owners Group Rept, Utility Resolution Guidance of ECCS Suction Strainer Blockage ML20212J0451999-09-21021 September 1999 Forwards Safety Evaluation of Licensee USI A-46 Program at Quad Cities Nuclear Power Station,Units 1 & 2,established in Response to GL 87-02 Through 10CFR50.54(f) Ltr ML20212D8231999-09-20020 September 1999 Informs That Effectieve 991101,NRC Region III Will Be Conducting Safety System Design & Performance Capability Pilot Insp at Quad Cities Nuclear Power Station.Insp Will Be Performed IAW NRC Pilot Insp Procedure 71111-21 ML20212C6961999-09-15015 September 1999 Forwards Insp Repts 50-254/99-17 & 50-265/99-17 on 990823- 0827.No Violations Noted SVP-99-190, Clarifies Statement Contained in NRC Insp Repts 50-254/99-12 & 50-265/99-12,dtd 990813,paragraph 4OA1.3B, Observation & Findings, Re Sys Mod to DG Air Start Sys1999-09-13013 September 1999 Clarifies Statement Contained in NRC Insp Repts 50-254/99-12 & 50-265/99-12,dtd 990813,paragraph 4OA1.3B, Observation & Findings, Re Sys Mod to DG Air Start Sys ML20211Q7961999-09-0909 September 1999 Forwards Correction to Administrative Error on Page 8 of NRC Insp Repts 50-254/99-16 & 50-265/99-16,transmitted by Ltr, ML20217H5661999-09-0909 September 1999 Discusses 990907 Pilot Plan Mgt Meeting Re Results to-date of Pilot Implementation of NRC Revised Reactor Oversight Process at Prairie Island & Quad Cities.Agenda & Handouts Provided by Utils Encl ML20211Q6511999-09-0808 September 1999 Informs That NRC Tentatively Scheduled Initial Licensing Exam for Quad Cities Operator License Applicants During Wk of 000327.Validation of Exam Will Occur at Station During Wk of 000306 ML20211G1221999-08-27027 August 1999 Forwards fitness-for-duty Program Performance Data for Each of Comm Ed Nuclear Power Stations & Corporate Support Employees within Scope of Rule for six-month Period Ending 990630,IAW 10CFR26.71(d) ML20211F8251999-08-25025 August 1999 Forwards Insp Repts 50-254/99-15 & 50-265/99-15 on 990816-20.No Violations Noted.Insp Evaluated Effectiveness of Maint Rule Program & Review Periodic Evaluation Specifically Required for 10CFR50.65 ML20211B8691999-08-20020 August 1999 Forwards Insp Repts 50-254/99-10,50-265/99-10,50-454/99-09, 50-455/99-09,50-456/99-10 & 50-457/99-10 on 990628-0721. Action Plans Developed to Address Configuration Control Weaknesses Not Totally Effective as Listed ML20211D1491999-08-19019 August 1999 Forwards Insp Repts 50-254/99-16 & 50-265/99-16 on 990719-22.Staff Identified Major Discrepancy Re Accuracy of Data Submitted to NRC for Protected Area Security Equipment Performance ML20211C7601999-08-19019 August 1999 Confirms NRC Intent to Meet with NSP & Ceco on 990807 in Lisle,Il to Discuss with Region III Pilot Plants,Any Observations,Feedback,Lessons Learned & Recommendations Relative to Implementation of Pilot Program ML20210R7451999-08-13013 August 1999 Forwards Insp Repts 50-254/99-11 & 50-265/99-11 on 990601-0720.NRC Identified Several Issues Which Were Categorized as Being of Low Risk Significance.Two Issues Involved NCVs of Regulatory Requirements SVP-99-147, Notifies of Change to Bases of TS to Licenses DPR-29 & DPR- DPR-30.Change to TS Section 3/4.9 Provides Clarity & Consistency with Sys Design Description in Ufsar,Sections 8.3.2.1 & 8.3.2.2.TS Bases Page,Encl1999-08-13013 August 1999 Notifies of Change to Bases of TS to Licenses DPR-29 & DPR- DPR-30.Change to TS Section 3/4.9 Provides Clarity & Consistency with Sys Design Description in Ufsar,Sections 8.3.2.1 & 8.3.2.2.TS Bases Page,Encl SVP-99-170, Forwards Relief Requests CR-25,CR-26,CR-27,CR-28,PR-11, PR-12 & PR-13,on Basis That Compliance with Specified Requirements Would Result in Hardship or Unusual Difficulty Without Compensating Increase in Level of Quality & Safety1999-08-13013 August 1999 Forwards Relief Requests CR-25,CR-26,CR-27,CR-28,PR-11, PR-12 & PR-13,on Basis That Compliance with Specified Requirements Would Result in Hardship or Unusual Difficulty Without Compensating Increase in Level of Quality & Safety ML20210T9941999-08-13013 August 1999 Forwards Insp Repts 50-254/99-12 & 50-265/99-12 on 990628-0716.Violations Noted SVP-99-154, Notifies NRC That M Price,License SOP-31389,is No Longer Required to Maintain Operator License.Price Was Removed from Licensed Duty on 990729 & Comm Ed Requests License Be Terminated1999-08-13013 August 1999 Notifies NRC That M Price,License SOP-31389,is No Longer Required to Maintain Operator License.Price Was Removed from Licensed Duty on 990729 & Comm Ed Requests License Be Terminated ML20210R9541999-08-10010 August 1999 Informs That During 990804 Telcon Between J Bartlet & M Bielby,Arrangements Were Made for NRC to Insp License Operator Requalification Program at Plant.Insp Planned for Wks of 991018 & 25 ML20210N5651999-08-0606 August 1999 Forwards Rev 8 to Nuclear Generating Stations Emergency Plan, for Plants.With Summary of Changes ML20210M5461999-08-0606 August 1999 Discusses 990804 Telcon Between J Bartlet & M Bielby,Where Arrangements Were Made for NRC to Inspect Licensed Operator Requalification Program at Plant.Insp Planned for Wks of 991018 & 25 ML20210M9131999-08-0202 August 1999 Forwards Response to NRC AL 99-02, Operating Reactor Licensing Action Estimates, for Fys 2000 & 2001 for Comed ML20210L8371999-08-0202 August 1999 Forwards SE Accepting Licensee 60-day Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety Related Motor-Operated Valves ML20210M4691999-07-30030 July 1999 Forwards Insp Repts 50-254/99-14 & 50-265/99-14 on 990713-15.One NCV Was Identified & Discussed in Encl Insp ML20210H4661999-07-29029 July 1999 Forwards Insp Repts 50-254/99-13 & 50-265/99-13 on 990628-0702.No Violations Noted.Insp Consisted of Selective Examination of Procedures & Representative Records, Observations of Activities & Interviews with Personnel 05000254/LER-1999-002, Forwards LER 99-002-01,IAW 10CFR50.73(a)(2)(iv).Rev Includes Cause Codes & Energy Industry Identification Sys Identifiers Which Were Erroneously Omitted in Original Ler.Commitments Listed1999-07-29029 July 1999 Forwards LER 99-002-01,IAW 10CFR50.73(a)(2)(iv).Rev Includes Cause Codes & Energy Industry Identification Sys Identifiers Which Were Erroneously Omitted in Original Ler.Commitments Listed SVP-99-151, Responds to NRC 990701 Telcon RAI Re Licensee Amend Request Re Use of Containment Overpressure to Support NPSH Available for ECCS at Quad Cities Nuclear Power Station,Units 1 & 21999-07-23023 July 1999 Responds to NRC 990701 Telcon RAI Re Licensee Amend Request Re Use of Containment Overpressure to Support NPSH Available for ECCS at Quad Cities Nuclear Power Station,Units 1 & 2 SVP-99-150, Forwards Responses to 990520 RAI Re Annual 10CFR50.46 Rept1999-07-23023 July 1999 Forwards Responses to 990520 RAI Re Annual 10CFR50.46 Rept SVP-99-146, Informs of Termination of License SOP-31132-1,for G Green, as Required by 10CFR50.74(b).Individual Was Removed from License Duty on 9906251999-07-21021 July 1999 Informs of Termination of License SOP-31132-1,for G Green, as Required by 10CFR50.74(b).Individual Was Removed from License Duty on 990625 ML20210B7071999-07-16016 July 1999 Responds to Requesting Review & Approval of Three Proposed Changes to Ceco QA TR,CE-1A Per 10CFR50.54(a)(3) & 10CFR50.4(b)(7) ML20196J9061999-07-0101 July 1999 Provides Evidence That Util Maintains Guarantee of Payment of Deferred Premiums in Amount of $10 Million for Each of Thirteen Reactors,Per 10CFR140.21 ML20196J9131999-07-0101 July 1999 Submits Status of Nuclear Property Insurance Currently Maintained for Braidwood,Byron,Dresden,Lasalle County,Quad Cities & Zion Nuclear Power Stations,Per 10CFR50.54(w)(3) ML20209B8241999-06-30030 June 1999 Forwards Five 3.5 Inch Computer Diskettes Containing Revised Annual Dose Repts for 1994 Through 1998 for Individuals Receiving Neutron Dose Not Previously Included in Reported Total Effective Dose Equivalent Values.Without Diskettes SVP-99-139, Forwards Revised Action 2 & Associated TS Bases Changes, Describing Specific Alternate Method for Determining Drywell Floor Drain Sump Leakage1999-06-30030 June 1999 Forwards Revised Action 2 & Associated TS Bases Changes, Describing Specific Alternate Method for Determining Drywell Floor Drain Sump Leakage ML20209B2081999-06-29029 June 1999 Discusses Closure of Response to RAI Re GL 92-01,Rev 1,Suppl 1, Reactor Vessel Structural Integrity. Rvid,Version 2 Issued as Result of Review of Responses.Info Should Be Reviewed & Comments Submitted by 990901 05000265/LER-1999-002, Forwards LER 99-002-00 for Quad Cities Nuclear Power Station IAW Requirements of 10CFR50.73(a)(2)(i)(B).Util Commits to One Listed Action1999-06-25025 June 1999 Forwards LER 99-002-00 for Quad Cities Nuclear Power Station IAW Requirements of 10CFR50.73(a)(2)(i)(B).Util Commits to One Listed Action SVP-99-122, Forwards Regulatory Commitment Change Summary Rept, Containing Summary Info from 980601 Through 9906011999-06-25025 June 1999 Forwards Regulatory Commitment Change Summary Rept, Containing Summary Info from 980601 Through 990601 SVP-99-066, Informs That J Reed,License SOP-31034-1,was Removed from License Duty in 990618.Termination of License Is Requested1999-06-25025 June 1999 Informs That J Reed,License SOP-31034-1,was Removed from License Duty in 990618.Termination of License Is Requested SVP-99-103, Informs NRC of Results of Subject Evaluation as Committed to in .Evaluation Consisted of Analytically Demonstrating That Cfu Factor for Rv Head Closure Studs Will Remain Below 1.0 for Remainder of Current License Period1999-06-25025 June 1999 Informs NRC of Results of Subject Evaluation as Committed to in .Evaluation Consisted of Analytically Demonstrating That Cfu Factor for Rv Head Closure Studs Will Remain Below 1.0 for Remainder of Current License Period ML20196F7921999-06-24024 June 1999 Forwards Meeting Summary,Nrc Meeting Handout & Licensee Handout from 990608 Meeting ML20196E7131999-06-23023 June 1999 Forwards Insp Repts 50-254/99-09 & 50-265/99-09 on 990421-0531.One Violation of NRC Requirements Occurred & Being Treated as non-cited Violation,Consistent with App C of Enforcement Policy ML20196E4821999-06-21021 June 1999 Discusses 990617 Meeting by Region III Senior Reactor Analysts (SRA) in Cordova,Il to Meet with PRA Staff to Discuss Initiatives in Risk Area & to Establish Dialog Between SRAs & PRA Staff 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARSVP-99-181, Forwards Biennial Update to Quad Cities Ufsar,Iaw 10CFR50.71(e).Update Includes Changes to Facility & Procedures & Are Current Through 9906301999-10-20020 October 1999 Forwards Biennial Update to Quad Cities Ufsar,Iaw 10CFR50.71(e).Update Includes Changes to Facility & Procedures & Are Current Through 990630 ML20217H4661999-10-18018 October 1999 Forwards Changes to EPIPs IAW 10CFR50.54(q) & 10CFR50,App E, Section V.Details of Changes Encl ML20217K7011999-10-13013 October 1999 Provides Response to Questions Related to Request for License Amend,Per 10CFR50.90, Credit for Containment Overpressure. Supporting Calculations Encl 05000254/LER-1999-004, Forwards LER 99-004-00,IAW Requirements of 10CFR50.73(a)(2)(i)(B).Util Is Committed to Listed Action1999-10-12012 October 1999 Forwards LER 99-004-00,IAW Requirements of 10CFR50.73(a)(2)(i)(B).Util Is Committed to Listed Action 05000254/LER-1999-003, Forwards LER 99-003-00 IAW 10CFR73(a)(2)(v)(A).Commitment Made by Util,Listed.Any Other Actions Described in LER Represent Intended or Planned Actions by Licensee1999-10-0707 October 1999 Forwards LER 99-003-00 IAW 10CFR73(a)(2)(v)(A).Commitment Made by Util,Listed.Any Other Actions Described in LER Represent Intended or Planned Actions by Licensee ML20216J8241999-09-30030 September 1999 Notifies of Removal of NRC Headquarters & Region III Offices from Controlled Copy Distribution of Certain CE Documents. Specific Documents,Associated Controlled Copy Numbers & NRC Location Affected Are Shown on Attachment to Ltr SVP-99-189, Confirms Completion of Actions Identified During Review of NRC Safety Evaluation of Boiling Water Reactor Owners Group Rept, Utility Resolution Guidance of ECCS Suction Strainer Blockage1999-09-22022 September 1999 Confirms Completion of Actions Identified During Review of NRC Safety Evaluation of Boiling Water Reactor Owners Group Rept, Utility Resolution Guidance of ECCS Suction Strainer Blockage SVP-99-190, Clarifies Statement Contained in NRC Insp Repts 50-254/99-12 & 50-265/99-12,dtd 990813,paragraph 4OA1.3B, Observation & Findings, Re Sys Mod to DG Air Start Sys1999-09-13013 September 1999 Clarifies Statement Contained in NRC Insp Repts 50-254/99-12 & 50-265/99-12,dtd 990813,paragraph 4OA1.3B, Observation & Findings, Re Sys Mod to DG Air Start Sys ML20211G1221999-08-27027 August 1999 Forwards fitness-for-duty Program Performance Data for Each of Comm Ed Nuclear Power Stations & Corporate Support Employees within Scope of Rule for six-month Period Ending 990630,IAW 10CFR26.71(d) SVP-99-154, Notifies NRC That M Price,License SOP-31389,is No Longer Required to Maintain Operator License.Price Was Removed from Licensed Duty on 990729 & Comm Ed Requests License Be Terminated1999-08-13013 August 1999 Notifies NRC That M Price,License SOP-31389,is No Longer Required to Maintain Operator License.Price Was Removed from Licensed Duty on 990729 & Comm Ed Requests License Be Terminated SVP-99-170, Forwards Relief Requests CR-25,CR-26,CR-27,CR-28,PR-11, PR-12 & PR-13,on Basis That Compliance with Specified Requirements Would Result in Hardship or Unusual Difficulty Without Compensating Increase in Level of Quality & Safety1999-08-13013 August 1999 Forwards Relief Requests CR-25,CR-26,CR-27,CR-28,PR-11, PR-12 & PR-13,on Basis That Compliance with Specified Requirements Would Result in Hardship or Unusual Difficulty Without Compensating Increase in Level of Quality & Safety SVP-99-147, Notifies of Change to Bases of TS to Licenses DPR-29 & DPR- DPR-30.Change to TS Section 3/4.9 Provides Clarity & Consistency with Sys Design Description in Ufsar,Sections 8.3.2.1 & 8.3.2.2.TS Bases Page,Encl1999-08-13013 August 1999 Notifies of Change to Bases of TS to Licenses DPR-29 & DPR- DPR-30.Change to TS Section 3/4.9 Provides Clarity & Consistency with Sys Design Description in Ufsar,Sections 8.3.2.1 & 8.3.2.2.TS Bases Page,Encl ML20210N5651999-08-0606 August 1999 Forwards Rev 8 to Nuclear Generating Stations Emergency Plan, for Plants.With Summary of Changes ML20210M9131999-08-0202 August 1999 Forwards Response to NRC AL 99-02, Operating Reactor Licensing Action Estimates, for Fys 2000 & 2001 for Comed 05000254/LER-1999-002, Forwards LER 99-002-01,IAW 10CFR50.73(a)(2)(iv).Rev Includes Cause Codes & Energy Industry Identification Sys Identifiers Which Were Erroneously Omitted in Original Ler.Commitments Listed1999-07-29029 July 1999 Forwards LER 99-002-01,IAW 10CFR50.73(a)(2)(iv).Rev Includes Cause Codes & Energy Industry Identification Sys Identifiers Which Were Erroneously Omitted in Original Ler.Commitments Listed SVP-99-150, Forwards Responses to 990520 RAI Re Annual 10CFR50.46 Rept1999-07-23023 July 1999 Forwards Responses to 990520 RAI Re Annual 10CFR50.46 Rept SVP-99-151, Responds to NRC 990701 Telcon RAI Re Licensee Amend Request Re Use of Containment Overpressure to Support NPSH Available for ECCS at Quad Cities Nuclear Power Station,Units 1 & 21999-07-23023 July 1999 Responds to NRC 990701 Telcon RAI Re Licensee Amend Request Re Use of Containment Overpressure to Support NPSH Available for ECCS at Quad Cities Nuclear Power Station,Units 1 & 2 SVP-99-146, Informs of Termination of License SOP-31132-1,for G Green, as Required by 10CFR50.74(b).Individual Was Removed from License Duty on 9906251999-07-21021 July 1999 Informs of Termination of License SOP-31132-1,for G Green, as Required by 10CFR50.74(b).Individual Was Removed from License Duty on 990625 ML20196J9061999-07-0101 July 1999 Provides Evidence That Util Maintains Guarantee of Payment of Deferred Premiums in Amount of $10 Million for Each of Thirteen Reactors,Per 10CFR140.21 ML20196J9131999-07-0101 July 1999 Submits Status of Nuclear Property Insurance Currently Maintained for Braidwood,Byron,Dresden,Lasalle County,Quad Cities & Zion Nuclear Power Stations,Per 10CFR50.54(w)(3) ML20209B8241999-06-30030 June 1999 Forwards Five 3.5 Inch Computer Diskettes Containing Revised Annual Dose Repts for 1994 Through 1998 for Individuals Receiving Neutron Dose Not Previously Included in Reported Total Effective Dose Equivalent Values.Without Diskettes SVP-99-139, Forwards Revised Action 2 & Associated TS Bases Changes, Describing Specific Alternate Method for Determining Drywell Floor Drain Sump Leakage1999-06-30030 June 1999 Forwards Revised Action 2 & Associated TS Bases Changes, Describing Specific Alternate Method for Determining Drywell Floor Drain Sump Leakage SVP-99-103, Informs NRC of Results of Subject Evaluation as Committed to in .Evaluation Consisted of Analytically Demonstrating That Cfu Factor for Rv Head Closure Studs Will Remain Below 1.0 for Remainder of Current License Period1999-06-25025 June 1999 Informs NRC of Results of Subject Evaluation as Committed to in .Evaluation Consisted of Analytically Demonstrating That Cfu Factor for Rv Head Closure Studs Will Remain Below 1.0 for Remainder of Current License Period SVP-99-122, Forwards Regulatory Commitment Change Summary Rept, Containing Summary Info from 980601 Through 9906011999-06-25025 June 1999 Forwards Regulatory Commitment Change Summary Rept, Containing Summary Info from 980601 Through 990601 05000265/LER-1999-002, Forwards LER 99-002-00 for Quad Cities Nuclear Power Station IAW Requirements of 10CFR50.73(a)(2)(i)(B).Util Commits to One Listed Action1999-06-25025 June 1999 Forwards LER 99-002-00 for Quad Cities Nuclear Power Station IAW Requirements of 10CFR50.73(a)(2)(i)(B).Util Commits to One Listed Action SVP-99-066, Informs That J Reed,License SOP-31034-1,was Removed from License Duty in 990618.Termination of License Is Requested1999-06-25025 June 1999 Informs That J Reed,License SOP-31034-1,was Removed from License Duty in 990618.Termination of License Is Requested SVP-99-125, Forwards Technical Info Re ECCS Suction Strainers at Quad Cities Nuclear Power Station Units 1 & 2,to Support Review of 990129 Lar.Rev 0 to TR-VQ1500-02, Clean ECCS Suction Strainer Head Loss Test Rept, Encl1999-06-15015 June 1999 Forwards Technical Info Re ECCS Suction Strainers at Quad Cities Nuclear Power Station Units 1 & 2,to Support Review of 990129 Lar.Rev 0 to TR-VQ1500-02, Clean ECCS Suction Strainer Head Loss Test Rept, Encl ML20195E3491999-06-0707 June 1999 Withdraws Util Requesting License Change for Plant Security Plan Rev.Licensee Will re-evaluate Situation & May Request Approval of Change in Future ML20207G1451999-06-0707 June 1999 Forwards Rev 45 to Comed Quad Cities Nuclear Power Station Security Plan.Rev Includes Changes Listed.Security Plan Is Withheld from Public Disclosure Per 10CFR73.21 ML20195D6351999-06-0404 June 1999 Notifies NRC of Actions That Has Been Taken in Accordance with 10CFR26, Fitness for Duty Programs SVP-99-105, Informs NRC of Rev to Schedule for Completing Setpoint/ Uncertainty Calculations & Procedure Changes,Originally Planned for Completion on 9905291999-05-20020 May 1999 Informs NRC of Rev to Schedule for Completing Setpoint/ Uncertainty Calculations & Procedure Changes,Originally Planned for Completion on 990529 ML20195B2301999-05-19019 May 1999 Requests Approval of Proposed Changes to QA Topical Rept CE-1-A,rev 66a.Attachment a Describes Changes,Reason for Change & Basis for Concluding That Revised QAP Incorporating Proposed Changes Continues to Satisfy 10CFR50AppB SVP-99-111, Informs NRC of Current Status of Actions on Response to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design-Basis Accident Conditions1999-05-17017 May 1999 Informs NRC of Current Status of Actions on Response to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design-Basis Accident Conditions SVP-99-098, Fulfills Thirty Day & Annual Reporting Requirements of 10CFR50.46 for Plant.Eccs Evaluation Change Rept Transmitted in Entirety,Fulfilling Thirty Day & Annual Reporting Requirements Specified in 10CFR50.46(a)(3)(i)1999-05-17017 May 1999 Fulfills Thirty Day & Annual Reporting Requirements of 10CFR50.46 for Plant.Eccs Evaluation Change Rept Transmitted in Entirety,Fulfilling Thirty Day & Annual Reporting Requirements Specified in 10CFR50.46(a)(3)(i) SVP-99-099, Requests Relief from Requirements of 10CFR50.55a(g) Re Submittal of Relief Requests for Those Welds for Which Examinations of Greater than 90% of Weld Vol Was Not Acheived During 2nd ISI Program Interval1999-05-13013 May 1999 Requests Relief from Requirements of 10CFR50.55a(g) Re Submittal of Relief Requests for Those Welds for Which Examinations of Greater than 90% of Weld Vol Was Not Acheived During 2nd ISI Program Interval SVP-99-096, Provides Suppl Response to Violations Noted in Insp Repts 50-254/98-20 & 50-265/98-23.Corrective Actions:Listed Multidiscipline Team Will Perform self-assessment IAW Station Program for self-assessments in May 19991999-05-12012 May 1999 Provides Suppl Response to Violations Noted in Insp Repts 50-254/98-20 & 50-265/98-23.Corrective Actions:Listed Multidiscipline Team Will Perform self-assessment IAW Station Program for self-assessments in May 1999 05000254/LER-1999-001, Forwards LER 99-001-00 for Quad Cities Nuclear Power Station.Licensee Shall Rept Any Operation or Condition Prohibited by Plant Tech Specs.Util Committing to Listed Actions1999-05-12012 May 1999 Forwards LER 99-001-00 for Quad Cities Nuclear Power Station.Licensee Shall Rept Any Operation or Condition Prohibited by Plant Tech Specs.Util Committing to Listed Actions ML20206F5381999-04-30030 April 1999 Forwards Magnetic Tape Containing Annual Dose Repts for 1998 for Braidwood,Byron,Dresden,Lasalle County,Quad Cities & Zion Nuclear Power Stations,Per 10CFR20.2206(c).Without Magnetic Tape SVP-99-108, Forwards Quad Cities 1998 Radiological Environ Operating Rept, IAW Plant TS 6.9.A.3.Rept Contains Results of Radiological Environ & Meteorological Monitoring Programs. Radioactive Effluent Release Rept Was Submitted 9903301999-04-30030 April 1999 Forwards Quad Cities 1998 Radiological Environ Operating Rept, IAW Plant TS 6.9.A.3.Rept Contains Results of Radiological Environ & Meteorological Monitoring Programs. Radioactive Effluent Release Rept Was Submitted 990330 SVP-99-036, Forwards Reg Guide 1.16 Rept Number of Personnel-Rem by Work & Job Function for 1998. Associated Collective Deep Dose Equivalent Reported According to Work & Job Functions1999-04-29029 April 1999 Forwards Reg Guide 1.16 Rept Number of Personnel-Rem by Work & Job Function for 1998. Associated Collective Deep Dose Equivalent Reported According to Work & Job Functions SVP-99-088, Informs That Util Is Withdrawing IST Relief Rquests RV-02B & RV-03B1999-04-29029 April 1999 Informs That Util Is Withdrawing IST Relief Rquests RV-02B & RV-03B ML20205T1141999-04-22022 April 1999 Provides Comments from Technical Review of Draft Info Notice Re Unanticipated Reactor Water Draindown at Quad Cities Nuclear Power Station,Unit 2,ANO,Unit 2 & JAFNPP ML20206B2471999-04-20020 April 1999 Informs That SE Kuczynski Has Been Transferred to Position No Longer Requiring SRO License.Cancel License SOP-31030-1, Effective 990412 SVP-99-065, Requests That License SOP-31516,for Jf Graham,Be Terminated, Per 10CFR50.74(b).Individual Was Removed from License Duty on 990319 & No Longer Requires Operator License1999-04-14014 April 1999 Requests That License SOP-31516,for Jf Graham,Be Terminated, Per 10CFR50.74(b).Individual Was Removed from License Duty on 990319 & No Longer Requires Operator License SVP-99-058, Submits Plant Specific ECCS Evaluation Changes,Per Annual Reporting Requirements of 10CFR50.46.Attachments Include Current Assessment Data Re PCT Info Limiting LOCA Evaluations1999-04-14014 April 1999 Submits Plant Specific ECCS Evaluation Changes,Per Annual Reporting Requirements of 10CFR50.46.Attachments Include Current Assessment Data Re PCT Info Limiting LOCA Evaluations SVP-99-063, Responds to NRC Re Violations Noted in Insp Repts 50-254/98-21 & 50-265/98-21.Corrective Actions:Revised Site ISI Procedure Qcap 0410-06, ISI Plan Implementation for Third Ten Year Insp Interval1999-04-0909 April 1999 Responds to NRC Re Violations Noted in Insp Repts 50-254/98-21 & 50-265/98-21.Corrective Actions:Revised Site ISI Procedure Qcap 0410-06, ISI Plan Implementation for Third Ten Year Insp Interval JAFP-99-0129, Submits Comments on Technical Review of Draft Info Notice Describing Unanticipated Reactor Water Draindown at Quad Cities Unit 2,ANO & FitzPatrick1999-04-0909 April 1999 Submits Comments on Technical Review of Draft Info Notice Describing Unanticipated Reactor Water Draindown at Quad Cities Unit 2,ANO & FitzPatrick SVP-99-057, Notifies of Change to Bases for TSs Section 3/4.5, ECCS, Re1999-04-0505 April 1999 Notifies of Change to Bases for TSs Section 3/4.5, ECCS, Re ML20205K5841999-03-31031 March 1999 Submits Rept on Status of Decommissioning Funding for Reactors Owned by Comm Ed.Attachment 1 Contains Amount of Decommissioning Funds Estimated to Be Required Pursuant to 10CFR50.75(b) & (C) SVP-99-062, Informs NRC of Rev to Schedule for Analytically Demonstrating That Cumulative Usage Factor for Reactor Vessel Head Closure Studs Will Remain Below 1.0 for Remainder of Current License Period1999-03-31031 March 1999 Informs NRC of Rev to Schedule for Analytically Demonstrating That Cumulative Usage Factor for Reactor Vessel Head Closure Studs Will Remain Below 1.0 for Remainder of Current License Period 1999-09-30
[Table view] |
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(" xv J Downers Grove, lHinois 00515 I January 25, 1991 Dr. Thomas E. Hurley, Director Office of Nuclear Reactor Regulation U.S. Nuclear Regulatory Commission Washington, D.C. 20555 Attn: Document Control Desk
Subject:
Quad Cities Nuclear Power Station Units 1 and 2 Request for Exemption of the Feedwater Check Valves from 10 CFR 50 Appendix J Test Program N RC.. Doc heL ho sm 5.0: 25L and_. 50- 265 Dr. Murley:
On September 25, 1990 members of the Commonwealth Edison's and Nuclear Regulatory Commission's (including Region III and NRR representatives) staffs conducted a meeting to discuss Commonwealth Edison's actions to improve the performance of containment valves during 10 CFR 50 Appendix J testing at Quad Cities Station. During that meeting, Commonwealth Edison proposed to submit a request to exempt the feedwater check valves from the Appendix J Test Program. The basis for this request is a calculation, which demonstrates that water remains in the feedwater line following a loss-of-coolant accident.
1 During the September 25, 1990 meeting, Commonwealth Edison provided an l overview of Quad Cities Station's request. The NRR representative indicated that the request was reasonable and should be formally submitted.
In lieu of performing an air test of the feedwater check valves, Commonwealth Edison proposes to perform a water leakage test of the valves to ensure water remains in the piping between the reactcr vessel and feedwater valves. This request does not involve a change to the Technical Specifications or Final St.fety Analysis Report.
If there are any questions or comments regarding this submittal, please contact me at 708/515-7283.
Very truly yours, l
Rita Stols 310019 Nuclear Licensing Administrator RS:Imw 91ozololy fy@ h s4
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Dr. T.E. Hurley January 25, 1991 Attachments A: Request for Exemption of the Feedwater Check Valves from the requirements of 10CFR50 Appendix J B: Safety Evaluation by the Office of Nuclear Reactor Regulation Supporting Amendments 164 and 101 to facility Operating Licenses DPR-57 and NPF-5.
C: Feedwater Line Thermal Hydraulic Behavior during LOCA conditions for Quad Cities Nuclear Power Station, RSA-0-90-03 dated November 21, 1990.
Figures 1: Feedwater Piping Inside the Drywell 2: Feedwater Piping Outside the Drywell 3: Condensate and feedwater System 4: FSAR Figure 5.2.17 " Containment Pressure Response following Design Basis Loss-of-Coolant Accident" cc: A ?. Davis, Regional Administrator, RIII L.N. 01shan, Project Manager, NRR J.A. Ludrick, Technical Staff, NRR f.A. Maura, Inspector, Region III T. Taylor, Senior Resident Inspector ZNLD702/4
i 4 AUACHMEXLA QUADSLI1ESJUCLEAR POWER STAI1QM REQUESL10R_EXEMEIION_Of_THE_EEEDMIEILCHECLVALVES EROK_10_CffL50_AEEEM0lLJ_TISLREQUIREMENLS
Background
On June 15, 1990, Region III issued the results of an inspection (50-254/89024; 50-265/89024) which was performed on the Quad Cities Station 10CFR50 Appendix J Test Program. As a result of the inspection, a Notice of Violation, which cited ineffective corrective actions to repetitive Appendix J test failures, was issued. Commonwealth Edison provided a response to the violation in a letter dated August 17, 1990. Sub:,equently, Region III requested that a meeting be conducted to discuss the response. On September 25, 1990, members of the Commonwealth Edison Company's and the i Nuclear Regulatory Commission's (including representatives from both Region III and Nuclear Reactor Regulation) staffs conducted that meeting.
During the September 25, 1990 meeting, Commonwealth Edison provided an update of the investigations which are underway to resolve the leakage pathway concerns. As a result of these investigations, Commonwealth Edison identified
'that Georgia Power's Plant Hatch requested and received NRC's approval for eliminating the feedwater check valves from the Plant Hatch's 10 CFR 50 Appendix J test program. The basis for the NRC's approval to remove the valves from the Appendix J test program was that water was present in the feedwater lines during post accident condttions. At the time of the meeting, preliminary calculations confirmed that water would also be present in the feedwater lines following a loss-of-coolant accident (LOCA) at Quad Cities.
Commonwealth Edison proposed to submit a similar request for Quad Cities Station and provided a brief overview of the technical justification for the request. The NRR representative indicated that the request was reasonable and should be formally submitted.
Plant Hatch Request The basis for eliminating the feedwater chech valves from the 10 CFR 50 Appendix J Test Program at Plant Hatch was an analysis that demonstrated that water would remain in the feedwater lines between the vessel and inboard valve ,
following a loss-of-coolant accident (LOCA). In lieu of the Appendix J test, a stringent water leakage test is required to ensure that the lines are water filled following the LOCA. Since the lines are no longer potential air leakage pathways, the leakage is excluded from the 0.6 and 0.75 La alt leakage totals. A copy of the NRC's Safety Evaluation Report is contained in Attachment B for the Staff's reference, till.t'/ 7 N / B
l Quad Cities Station Request 10 CFR 50 Appendix J.Section II.il defines the valves which require Type C tests to include those that are in the feedwater piping. Commonwealth Edison requests the NRC's approval to discontinue Type C testing of the feedwater check valves on the basis that water remains in the feedwater line following the most limiting blowdown / fluid carryover event. Commonwealth Edison proposes to perform a water leakage test in lieu of the air test to assure water is maintained in the line.
Commonwealth Edison has performed an analysis for Quad Cities Station which examines the reactor vessel depressurization event and resultant feedwater line blowdown. The event was analyzed by the use of the computer code RELAP 5. A full six equation, two-phase calculation was performed to determine the amount of water which would remain in the feedwater line following reactor depressurization. Blowdown rates corresponding to a range of events, which included a small line break up to and including the design basis accident (DBA) of a recirculation system line break, were modeled. The analysis is contained in Attachment C.
Based on these calculations, the limiting event for feedwater system fluid carryover, which results in the least amount of water in the feedwater line, was the DBA recirculation line break. For this event, approximately 101 gallons of fluid remains in the feedwater line between the reactor vessel and the inboard feedwater check valve following reactor depressurization.
With the presence of water in essentially a vertical run of the feedwater line between the vessel and inboard check valve, it is not possible for any containment atmosphere to escape. A schematic drawing of the feedwater line inside containment is provided as figure 1.
In addition, a containment isolation function is also provided by a water seal which is created by a 15 foot elevation water head located between the heater outlet and the outboard feedwater check valve. (Reference Figure 2)
The elevation head exerts approximately 6.2 psi pressure on the outboard feedwater check valve. The feedwater line, therefore, remains sealed provided that containment pressure does not exceed 6.2 psi.
As indicated in FSAR Figure 5.2.17 " Containment Pressure Response following Design Basis Loss of Coolant Accident", containment pressure decays below 6.2 ps) in approximately 55.6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> following the initial reactor vessel blowdown. (Figure 5.2.17 is attached as Figure 4) Commonwealth Edison, therefore, proposes a minimum path water leakage rate test acceptance criteria for the inboard and outboard feedwater check valves of 1.82 gallons per hour to ensure that water remains in the feedwater line for 55.6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> following blowdown. Following the 55.6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> after reactor depressurization, the containment function will be performed by a water seal which is created by the 15 foot water head outside of containment.
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Currently, the feedwater line which is located inside of containment is 1 both seismic and safety-related piping. The feedwater piping, which is 1 4 outside of containment, meets seismic and safety-related requirements up to the outboard feedwater check valve. The majority of the feedwater piping i outside of containment, therefore, is non-seismic, non-safety related piping.
If the NRC Staff approves this request to exempt the feedwater check valves from the Appendix J Test Program, Commonwealth Edison will upgrade this piping to meet seismic and safety-related piping requirements.
Commonwealth Edison has also considered the case of the feedwater line break as the initiator to a event. This event is classified as a medium break loss-of-coolant accident. Containment isolation provisions were not I
- considered in this case due to the absence of resulting core damage.
In addition to the design features discussed above, other mitigating design features exist which support the removal of the feedwater check valves from the Appendix J Program:
- 1. _A third check valve exists upstream of each outboard feedwater check valve. The valve (located on the "B" line) is water tested as part of the In-Service Test Program. No credit is taken for the third valve in the calculation to determine the amount of water which remains in the feedwater line following reactor vessel depressurization.
- 2. The High Pressure Coolant Injection (HPCI) System is injected into the vessel through one of the feedwater lines. HPCI takes its suction from the Contaminated Storage Tanks; therefore, the temperature of the coolant in the feedwater Ilne would be reduced to less than 212 degrees Fahrenheit. The line, therefore, would remain filled with water.
- 3. The Reactor Core Injection Coolant (RCIC) System is injected into the vessel through the other feedwater line. The use of RCIC would assure that the line is water filled.
Conclusion The Quad Cities Technical Specifications or the Final Safety Analysis Report does not contain a listing of valves which are required to be tested per 10 CFR 50 Appendix J. This request, therefore, does not require a change to either document. Commonwealth Edison requests the NRC's approval to exempt the-feedwater check valves from the Appendix J Test Program, titLD/ 702 /*1
. If this request is approved:
- 1. Type C testing of the inboard and outboard feedwater check valves will continue until the outboard feedwater piping (up to the feedwater heaters) is upgraded to meet seismic and safety-related piping requirements. After the piping is upgraded, Type C tests would be discontinued on the valves.
- 2. Water leakage tests will be conducted (in lieu of the air test), at a pressure of Pa, on the inboard and outboard feedwater check valves. The acceptance criterla for this water leakage test will be established at 1.82 gallons per hour.
- 3. The requirement for inboard and outboard feedwater check valves water leakage test will be included in the In-Service Testing Program. The Program will be revised when the water leakage test commence on the feedwater check valves.
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SAFETY EVALUATION BY THE OFFICE.OF NUCLEAR REACTOR REGULATION SUPPORTING AMENDMENT NOS.16d AND 101 TO FACILITY OPERATING LICENSES DPR-57 AND NPF-5 GEORGIA POWER COMPANY OGLETHORPE POWER CORPORATION MUNICIPAL ELE URIC AUTHORITY OF GEORGIA CITY df DALTON. lEORGIA EDWIN 1. HATCH NUCLEAR PLANT. UNITS 1 AND 2 DOCKET NOS. 50-321 AND 50-366
1.0 INTRODUCTION
By letter dated February 3,1989, Georgia Power Conpany (the licensee) requested amendments to the Technical Specifications (TS) for the Edwin 1.
Hatch Nuclear Plant, Units 1 and 2. Specifically, the proposed amendments would modify the TS for Units 1 and 2 to: (1) Change the maximum operating times for certain primary containment isolation valves (PCIVs) to account for a different method of neasuring; (2) exclude several unit 1 containment penetrations and PCIVs from the local leak rate test (LLRT) program; (3) revise Unit 1 TS section 4.7 A.2 and Unit 2 TS section 4.6.1.3 to achieve similarity between the two documents, to comply with current 10 CFR 50 Appendix J testing requirements, and to specify an allowable leakage; (4) delete penetration 218A from Unit 1 TS Table 3.7-2; and (5) remove the isolation valves associated with the primary feedwater and the torus drainage and purification systems from Unit 2 TS section 3.6.1.2.
2.0 EVALUATION 2.1 Proposed Change 1 - Change the maximum operating times for certain primary containment isolation valves (PCIVs) to account for a different method of measuring.
The TS for Hatch Units 1 and 2 now contain table listings (Table 3.7-1 for Unit 1 and Table 3.6.3-1 for Unit 2) of power operated, automatically initiated PCIVs showing maximum operating times for isolating upon receipt of an appropriate signal. The operating times shown in the tables are based upon a
" light-to-light" measuring method, which was used during the plant functional testing prior to reactor startup. However, the ASME Code,Section XI, requires that valve stroke times be measured from initiation of the actuating signal to-the end of the actuating cycle, more connonly referred to as a
" switch-to-light" measuring method. The changes to the maximum stroke times proposed by the licensee are merely to account for the change in stroke time measurement from the " light-to-light" method to the "swtich-to-light" rethod.
Actual valve operation does not change and the new "switen-to-light' operating
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times maintain the primary' containment design bases as defined in the Unit 1 and Unit 2 Final Safety Analysis Reports. Since the actual valve operation )
remains the same, we find this proposed change to be acceptable.
2.2 Proposed Change 2 - Exclude Unit 1 valves 1E41-F021, F022, F040, and F049; valves 1E51-F001, F002, F028 and F040; and containment penetrations X-212, ,
X-213, X-214 and X-215 from the Appendix J LLRT (Type C) program. 1 The named valves and the associated containment penetrations are those serving the reactor core isolation cooling (RCIC) turbine exhaust and turbine drain -
lines, and the high pressure coolant injection (HPCI) turbine exhaust and drain lines. These exhaust and drain lines terminate in the torus below the water level of the suppression pool. Since the torus water level is ;
controlled within narrow limits at all times, continuous coverage of piping ~
terminations is assured, thus providing a water seal between the atmospheres irside and outside the torus. Under this condition Type C testing is not required by Appendix J. The licensee states, however, that leak rate testing of these valves will still be performed in accordance with Section XI of the ASME code as part of the inservice inspection (ISI) program.
- The staff previously has approved the exemption of certain valves and 4
associated penetrations from the Type C testing requirements based upon a similar argument that the piping involved terminated below the water level in 30, 1986; and Amendment #140, the Hatchtorus Unit(Amundment #131
- 1. June 5,1987 . ) Hatch Unit 1, October Accordingly, we find acceptable the licensee's proposal to exclude the listed l valves and associated penetrations from the Type C testing program, and the i deletion of these valves and penetrations from Unit 1 TS Table 3.7-4 I 2.3 Proposed Change 3 - Revise Unit 1- TS 4.7. A.2 and Unit 2 TS 4.6.1.3 to achieve similarity between the two documents, to comply with current 10 CFR Part 50, Appendix J testing requirements, and to specify an allowable leakage.
Appendix J, Section !!!.D.2.b requires that containment air locks be tasted at 6-month intervals after initial fuel loading at an internal pressure of not less than Pa. Air locks that are opened when containment integrity is required shall be tested within 3 days after being opened, at a test pressure as specified in the TS. For Hatch Units 1 and 2, Pa is 57.5 psig and the test pressure specified for the 3-day test requirement is at least 10 psig. The-existing Unit 1 TS provide no acceptance criteria for leakage resulting from the 3-day test, while Unit 2 states "no detectable seal leakage." Neither of these is suitable to meet the requirement of 10 CFR Part 50, Appendix J.-
Section !!!.D.2.b(iv), which requires that, "The acceptence criteria for air lock testing shall be stated in the Technical Specifications."
The change proposed by the licensee would amend Unit 1 TS 4.7. A.2 and Unit 2 TS 4.6.1.3 to achieve identical wording as regards the test -requirements for the containment air locks, both in conformance with the requirements of
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Appendix J, Sections !!!.D.2.b.(i), (ii), and (iii) and would state acceptance criteria for allowable lea'kage in accordance with Appendix J. Section
!!!.D.2.b(iv) for the leak tests.
For the full pressure (Pa) leak tests, the allowable leakage is 0.05 La. This acceptance criterion is now stated in the TS for each unit and would remain unchanged. .For the 3-day tests conducted at pressures < 10 psig, an I acceptable leakage for each set of dour seals would be siecified as 0.01 La.
This reduced leakage rate is comparable to reduced pressure leak rates previously reviewed and approved by the staff for other plants, and is acceptable.
Accordingly, we find the licensee's proposed TS modifications regarding the containment air locks acceptable.
2.4 Propow1 Change 4 - Delete penetration 218A from Unit 1 TS Table 3.7-2.
Amendment No.140, issued on June 5,1987, deleted penetration 218A from the !
listing of containment isolation valves subject to Appendix J leak rate j testing (TS Table 3.7-4). Penetration 218A should have been deleted from TS Table 3.7-2 (Testable Penetrations with Double 0-Ring Seals) at this same time. This proposed change would correct that oversight. The change is administrative in nature and is acceptable, 2.5 Proposed Change 5 - Delete the isolation valves associated with the '
primary feedwater and the torus drainage and purification systems from Unit 2 l TS 3.6.1.2. ;
10 CFR Part 50, Appendix J, Section !!!.C states the conditions under which certain containment isolation valves sealed with fluid may be excluded when '
determining the total cosined leakage rate.
Primary feedwater valves 2B21-F010A & B and 2B21-F077A & B (in penetrations 9A and 9B) are expected to remain covered by water following a design basis Loss-of-Coolant Accident (LOCA). Note 30 to Unit 2 FSAR Table 3.8-5 states that these valves are expected to remain covered by water following a design basis LOCA. Further, Note 8 to the same table states that the system remains filled with water post-LOCA, that the valves are tested with water, and that valve leakage is not included in the 0.60 La type B and C tests to determine total local leakage. These valves, therefore, should not have been listed in TS 3.6.1.2, and their removal from the listing merely amounts to an administrative-correction.
Unit 2 FSAR subsection 6.2.1.2.2 states that the torus drainage and purification system valves (2G57-F011 'and 2G51-F012), wbich may be open at the time of an accident, receive a signal to close, and that following closure a water seal is established by the suppression pool water. These valves thus will have no gaseous leakage and, in accordance with 10 CFR Part 50, Appendix J. Section !!!.C, they need not be considered in determining the cosined leakage rate. The removal of these valves from the listing in TS 3.6.1.2 is, therefore, acceptable.
, 4
. 3.0 EYllR0* ENTAL CONSIDERATION These amendments change a requirement with respect to installation or use of a f acility component located within the restricted area as defined in 10 CFR Part 20 and change surveillance requirements. The staff has determined that the anendments invoke no significant increase in the amounts, and no significant change in the types, of any effluents that may be released offsite, and that there is no significant increase in individual or cumulative occupational radiation exposure. The Comission has previously issued a proposed finding that the amendments involve no significant hazards consideration and there has been no public coment on such finding. Accordingly, the amenchents meet the eligibility criteria for categorical exclusion set forth in 10 CFR 551.22(c)(9).
Pursuant to 10 CFR 551.22(b), no environmental impact statement or environmental assessment need be prepared in connection with the issuance of the amendments.
4.0 CONCLUSION
The Comission made a proposed determination that the amendments involve no significant ha:ards consideration which was published in the Federal Register (41 FR 13765) on April 5,1989, and consulted with the state of Georgia. No public comments were received, and the state of Georgia did not have any -
comments.
We have concluded, based on the considerations discussed above, that: (1) there is reasonable assurance that the health and safety of the public will not be endangered by operation in the proposed manner, and (2) such activitias will be conducted in compliance with the Comission's regulations, and the issuance of the amendments will not be inimical to the comon defense and security or to the health and safety of the public.
Principal Contributor: Lawrence P. Crocker, PDIl-3/0RP-1/II Dated: June 20, 1989
-__.--_____.______.____m_ _ _ _ _ _ _ . _ _ _ _ _ _ _ . _ _ . _ _ _ _ _ - . _ - _ _
!, 4 DATED- -lune 20 1989 AMENDMENT NO.101 TO FACILITY OPERATlHG LICENSE NPF-5. EDVIN 1. MATCH UNIT 2
. AMENDMENT NO.164 'N) FACILITY OPERATING LICENSE DPR-57. EDWIN 1. HATCH, UNIT.I.
. DISTRIBitTION:
N NRC PDR=
Local . PDR .
PDIl-3 R/F Hatch R/F G. Lainas- 14-E-4 E. Adensam 14-H-3
- D' Matthews-
. 14-H-25 M. Rood- 14-H-25 L. Crocker 14-H-25 D. Hagan . HNBB-3302 T. Meek (8) P1-137 W. Jones P-130A ACRS(10)- P-135 OGC-WF- 15-B-18 ARM /LFMB AR-2015 GPA/PA 17-F-2 E.-Butcher 11-F-23 L. Reyes- RIl B. Grimes: 9-A-2 E. Jordan HNBB-3302 J. Craig 8- D- 1 0Fol i i 2
_ _ _ . _ _ _ . _ . _ . _ _ _ _ _ _ _ _