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| | issue date = 07/30/1987 | | | issue date = 07/30/1987 |
| | title = LER 87-014-00:on 870630,discovered That Auxiliary Feedwater (AFW) Could Be Lost to Operating Unit in Event of High Energy Line Break in Main Steam Valve House.Caused by Poor Review of AFW Supply.Review continuing.W/870730 Ltr | | | title = LER 87-014-00:on 870630,discovered That Auxiliary Feedwater (AFW) Could Be Lost to Operating Unit in Event of High Energy Line Break in Main Steam Valve House.Caused by Poor Review of AFW Supply.Review continuing.W/870730 Ltr |
| | author name = BENSON D L | | | author name = Benson D |
| | author affiliation = VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.) | | | author affiliation = VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.) |
| | addressee name = | | | addressee name = |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18153A2741999-03-29029 March 1999 LER 99-002-00:on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212 ML18153A2301998-03-0606 March 1998 LER 98-004-00:on 980206,fire Watch Was Released Prematurely Resulting in Violation of Ts.Caused by Inadequate Planning of Repair Activity.Work Orders Will Include Ref to Applicable Procedures Developed to Assist in Repairs ML18153A1421997-06-10010 June 1997 LER 97-001-01:on 970123,shutdown Occurred Due to Drain Line Weld Leak.Inspected & Tested Turbine Trip Actuation circuitry.W/970610 Ltr ML18153A0141996-07-0202 July 1996 LER 96-004-00:on 960606,turbine/reactor Trip Occurred.Caused by High Level in Steam Generator B.Placed Plant in Hot Shutdown Condition,Calculated Shutdown Margin & Monitored Critical Safety Function Status trees.W/960702 Ltr ML18153A4561996-05-0707 May 1996 LER 96-002-00:on 960408,EDG Fire Suppression Sys Declared Inoperable Due to Personnel Error.Submitted Station Deviation rept.W/960507 Ltr ML18153A7791995-10-0909 October 1995 LER 95-007-00:on 950912,boron Crystals & Corrosion Products Discovered Outside Diameter of Vessel.Caused by through-wall Leakage.Work Request Initiated,Engineering & Shift Supervisor notified.W/951009 Ltr ML18152A3501995-02-24024 February 1995 LER 94-008-02:on 940929,filter Beds Experienced Abnormal Losses in Efficiency for Removal of Methyl Iodide.Caused by Charcoal Degradation.Sampling Performed for Assurance That Filter Degradation occurred.W/950224 Ltr ML18153B2251995-02-0303 February 1995 LER 95-002-00:on 950110,smoke Detector Surveillance Was Missed Due to Administrative Process Error.Electrical Periodic Test O-EPT-0904-04 Was Performed Satisfactorily on 950110.W/950203 Ltr ML18153B0891994-09-0606 September 1994 Corrected LER 94-0087-00,reflecting That Filter 3A Replaced & Returned to Service on 940720 Following Testing in Accordance W/Ts 4.12 ML18153B3201993-09-16016 September 1993 LER 93-010-00:on 930821,unit 1 Shutdown for Planned Maint to Repair Leakage on B SG Channel Head Caused by Cracking of Weld Associated W/B SG Channel Head Drain Line.Performed RCS Leak rate.W/930916 Ltr ML18153C3921990-10-0505 October 1990 LER 90-012-00:on 900909,common Mode Failure Mechanism Due to Marine Growth Identified for Emergency Svc Water Pump. W/901005 Ltr ML18153C0211989-12-18018 December 1989 LER 89-014-00:on 891117,results of Containment Purge Leak Test Indicated That Containment Purge Supply Penetration Exceeded 10CFR50,App J Leakage Value.Caused by Worn Rubber Seating Matl.Seat Replaced & Surface cleaned.W/891218 Ltr ML18152B1131988-08-30030 August 1988 LER 88-023-00:on 880802,C Steam Generator Channel IV Steam Flow Failed to Low Flow Indication.Caused by Failed Multiplier/Divider Unit Power Supply Transformer.Technicians Called in & Placed Channels in Trip mode.W/880830 Ltr ML18152B0971988-08-16016 August 1988 LER 88-008-01:on 880309,low Head Safety Injection Pump Inoperable Due to Failed Motor Leads Caused by Improper Splicing.Leads Repaired & Motor Replaced & Tested satisfactorily.W/880816 Ltr ML18153B4961988-08-0101 August 1988 LER 88-021-00:on 880728,PORV Cycled Open & Then Closed. Caused by Overly Conservative Setpoint.Setpoint Changed. W/880801 Ltr ML18152B0621988-07-18018 July 1988 LER 88-019-00:on 880625,emergency Diesel Generator 1 Unintentionally Started.Caused by Technician Accidentally Shorting Fast Start Relay.Electrician Counseled to Proceed Cautiously When Installing jumpers.W/880718 Ltr ML20027B1801982-09-0909 September 1982 LER 82-090/01T-0:on 820826,during Sampling of Gas Stripper Surge Tank Gaseous Effluent,High Spike Observed on vent-vent Gaseous Monitor.Caused by Gas Leak Through Damaged Quick Disconnect on Vessel.Disconnects Will Be Replaced ML20049J5361982-03-0101 March 1982 LER 82-016/03L-0:on 820131,loss of Boric Acid Flow to Blender Observed While Attempting Blend to Vol Control Tank. Caused by Loss of Heat Tracing & Damaged Insulation Upstream of Flow Transmitter.Tracing Replaced ML20041A4381982-02-0808 February 1982 LER 82-006/03L-0:on 820119,alarm Setpoint for Radiation Monitor RM-GW-102 Exceeded Tech Spec Limit.Caused by Instrument Drift.Instrument Recalibr ML20011A3941981-10-0101 October 1981 LER 81-056/03L-0:on 810902,RCS Cold Leg Sample Valve Opened W/O Operator Action & Would Not Stay Closed.Caused by Failure of seal-in Limit Switch in Valve Operator.Lock Nuts Became Loose Due to Vibration & Valve Usage ML20005A3551981-06-26026 June 1981 LER 81-035/03L-0:on 810529,fuel Oil Transfer Pump 1B Suction valve,1-EE-14,was Found Closed.Caused by Personnel Error. Valve Opened ML19350A3251981-03-0909 March 1981 LER 81-014/03L-0:on 810212,RM-CC-106 Alarm Setpoint Found Outside Tech Spec.Caused by Personnel Error.Setpoints Reset ML18139B0501981-01-30030 January 1981 LER 81-002/03L-0:on 810105,PT-27A Revealed Loss of Heat Tracing for Panel 10 Circuits 1A & 1B & Panel 11 Circuit 4A. Caused by Open Heating Elements.Defective Heat Tracing Tape Replaced ML18139B0111981-01-15015 January 1981 LER 80-050/03L-0:on 801228,amp Reading for Circuit 13A Boron Injection Recirculation to Boric Acid Tank Panel 8 Was Below Acceptance Criteria.Caused by Failure of Heat Tracing Tape Due to Excessive Heat.Heat Tracing Design Change Initiated ML18139A9681981-01-0505 January 1981 LER 80-073/03L-0:on 801205,discrepancies Discovered in Documenting Performance of Periodic Tests PT-18.8 & 19.1. Caused by Operations Personnel Oversight.Personnel Reinstructed & Improved PT Mgt Sys Developed ML18139A7981980-10-31031 October 1980 LER 80-026/03L-0:on 801005,w/reactor at 100% Power & Redundant Low Head Safety Injection Pump Out of Svc for Maint,Operator Failed to Retest Operable Pump 2-SI-P-1a within Specified Time.Caused by Operator Oversight ML18139A2701980-05-22022 May 1980 LER 80-024/03L-0:on 800426,during Maint W/Unit at Cold Shutdown,Partially Drained ECCS Water Flowed to Reactor W/O Containment Integrity,Causing Excess Primary Sys Boron Concentration, ML18114A6361979-06-0101 June 1979 LER 79-019/03L-0 on 790510:while Securing Purging Operations,Valve MOV-100D Did Not Close.Caused by Bearing Failure W/Resultant Gear Malfunction.Parts Replaced & Valve Returned to Svc ML18114A6021979-05-22022 May 1979 LER 79-015/03L-0 on 790422:liquid Waste Disposal Radiation Monitor Failed to Give High Alarm & Trip Release Valve. Caused by Procedural Inadequacy.Procedures Modified ML18113A7091978-12-13013 December 1978 LER #78-034/01X-1 on 781101:noted That 17 Spare Process Piping Penetrations on Unit #1 & 23 on Unit #2 Were Not Capped in Auxiliary Bldg.Caused by Failure to Properly Complete Capping at End of Constr 1999-03-29
[Table view] Category:RO)
MONTHYEARML18153A2741999-03-29029 March 1999 LER 99-002-00:on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212 ML18153A2301998-03-0606 March 1998 LER 98-004-00:on 980206,fire Watch Was Released Prematurely Resulting in Violation of Ts.Caused by Inadequate Planning of Repair Activity.Work Orders Will Include Ref to Applicable Procedures Developed to Assist in Repairs ML18153A1421997-06-10010 June 1997 LER 97-001-01:on 970123,shutdown Occurred Due to Drain Line Weld Leak.Inspected & Tested Turbine Trip Actuation circuitry.W/970610 Ltr ML18153A0141996-07-0202 July 1996 LER 96-004-00:on 960606,turbine/reactor Trip Occurred.Caused by High Level in Steam Generator B.Placed Plant in Hot Shutdown Condition,Calculated Shutdown Margin & Monitored Critical Safety Function Status trees.W/960702 Ltr ML18153A4561996-05-0707 May 1996 LER 96-002-00:on 960408,EDG Fire Suppression Sys Declared Inoperable Due to Personnel Error.Submitted Station Deviation rept.W/960507 Ltr ML18153A7791995-10-0909 October 1995 LER 95-007-00:on 950912,boron Crystals & Corrosion Products Discovered Outside Diameter of Vessel.Caused by through-wall Leakage.Work Request Initiated,Engineering & Shift Supervisor notified.W/951009 Ltr ML18152A3501995-02-24024 February 1995 LER 94-008-02:on 940929,filter Beds Experienced Abnormal Losses in Efficiency for Removal of Methyl Iodide.Caused by Charcoal Degradation.Sampling Performed for Assurance That Filter Degradation occurred.W/950224 Ltr ML18153B2251995-02-0303 February 1995 LER 95-002-00:on 950110,smoke Detector Surveillance Was Missed Due to Administrative Process Error.Electrical Periodic Test O-EPT-0904-04 Was Performed Satisfactorily on 950110.W/950203 Ltr ML18153B0891994-09-0606 September 1994 Corrected LER 94-0087-00,reflecting That Filter 3A Replaced & Returned to Service on 940720 Following Testing in Accordance W/Ts 4.12 ML18153B3201993-09-16016 September 1993 LER 93-010-00:on 930821,unit 1 Shutdown for Planned Maint to Repair Leakage on B SG Channel Head Caused by Cracking of Weld Associated W/B SG Channel Head Drain Line.Performed RCS Leak rate.W/930916 Ltr ML18153C3921990-10-0505 October 1990 LER 90-012-00:on 900909,common Mode Failure Mechanism Due to Marine Growth Identified for Emergency Svc Water Pump. W/901005 Ltr ML18153C0211989-12-18018 December 1989 LER 89-014-00:on 891117,results of Containment Purge Leak Test Indicated That Containment Purge Supply Penetration Exceeded 10CFR50,App J Leakage Value.Caused by Worn Rubber Seating Matl.Seat Replaced & Surface cleaned.W/891218 Ltr ML18152B1131988-08-30030 August 1988 LER 88-023-00:on 880802,C Steam Generator Channel IV Steam Flow Failed to Low Flow Indication.Caused by Failed Multiplier/Divider Unit Power Supply Transformer.Technicians Called in & Placed Channels in Trip mode.W/880830 Ltr ML18152B0971988-08-16016 August 1988 LER 88-008-01:on 880309,low Head Safety Injection Pump Inoperable Due to Failed Motor Leads Caused by Improper Splicing.Leads Repaired & Motor Replaced & Tested satisfactorily.W/880816 Ltr ML18153B4961988-08-0101 August 1988 LER 88-021-00:on 880728,PORV Cycled Open & Then Closed. Caused by Overly Conservative Setpoint.Setpoint Changed. W/880801 Ltr ML18152B0621988-07-18018 July 1988 LER 88-019-00:on 880625,emergency Diesel Generator 1 Unintentionally Started.Caused by Technician Accidentally Shorting Fast Start Relay.Electrician Counseled to Proceed Cautiously When Installing jumpers.W/880718 Ltr ML20027B1801982-09-0909 September 1982 LER 82-090/01T-0:on 820826,during Sampling of Gas Stripper Surge Tank Gaseous Effluent,High Spike Observed on vent-vent Gaseous Monitor.Caused by Gas Leak Through Damaged Quick Disconnect on Vessel.Disconnects Will Be Replaced ML20049J5361982-03-0101 March 1982 LER 82-016/03L-0:on 820131,loss of Boric Acid Flow to Blender Observed While Attempting Blend to Vol Control Tank. Caused by Loss of Heat Tracing & Damaged Insulation Upstream of Flow Transmitter.Tracing Replaced ML20041A4381982-02-0808 February 1982 LER 82-006/03L-0:on 820119,alarm Setpoint for Radiation Monitor RM-GW-102 Exceeded Tech Spec Limit.Caused by Instrument Drift.Instrument Recalibr ML20011A3941981-10-0101 October 1981 LER 81-056/03L-0:on 810902,RCS Cold Leg Sample Valve Opened W/O Operator Action & Would Not Stay Closed.Caused by Failure of seal-in Limit Switch in Valve Operator.Lock Nuts Became Loose Due to Vibration & Valve Usage ML20005A3551981-06-26026 June 1981 LER 81-035/03L-0:on 810529,fuel Oil Transfer Pump 1B Suction valve,1-EE-14,was Found Closed.Caused by Personnel Error. Valve Opened ML19350A3251981-03-0909 March 1981 LER 81-014/03L-0:on 810212,RM-CC-106 Alarm Setpoint Found Outside Tech Spec.Caused by Personnel Error.Setpoints Reset ML18139B0501981-01-30030 January 1981 LER 81-002/03L-0:on 810105,PT-27A Revealed Loss of Heat Tracing for Panel 10 Circuits 1A & 1B & Panel 11 Circuit 4A. Caused by Open Heating Elements.Defective Heat Tracing Tape Replaced ML18139B0111981-01-15015 January 1981 LER 80-050/03L-0:on 801228,amp Reading for Circuit 13A Boron Injection Recirculation to Boric Acid Tank Panel 8 Was Below Acceptance Criteria.Caused by Failure of Heat Tracing Tape Due to Excessive Heat.Heat Tracing Design Change Initiated ML18139A9681981-01-0505 January 1981 LER 80-073/03L-0:on 801205,discrepancies Discovered in Documenting Performance of Periodic Tests PT-18.8 & 19.1. Caused by Operations Personnel Oversight.Personnel Reinstructed & Improved PT Mgt Sys Developed ML18139A7981980-10-31031 October 1980 LER 80-026/03L-0:on 801005,w/reactor at 100% Power & Redundant Low Head Safety Injection Pump Out of Svc for Maint,Operator Failed to Retest Operable Pump 2-SI-P-1a within Specified Time.Caused by Operator Oversight ML18139A2701980-05-22022 May 1980 LER 80-024/03L-0:on 800426,during Maint W/Unit at Cold Shutdown,Partially Drained ECCS Water Flowed to Reactor W/O Containment Integrity,Causing Excess Primary Sys Boron Concentration, ML18114A6361979-06-0101 June 1979 LER 79-019/03L-0 on 790510:while Securing Purging Operations,Valve MOV-100D Did Not Close.Caused by Bearing Failure W/Resultant Gear Malfunction.Parts Replaced & Valve Returned to Svc ML18114A6021979-05-22022 May 1979 LER 79-015/03L-0 on 790422:liquid Waste Disposal Radiation Monitor Failed to Give High Alarm & Trip Release Valve. Caused by Procedural Inadequacy.Procedures Modified ML18113A7091978-12-13013 December 1978 LER #78-034/01X-1 on 781101:noted That 17 Spare Process Piping Penetrations on Unit #1 & 23 on Unit #2 Were Not Capped in Auxiliary Bldg.Caused by Failure to Properly Complete Capping at End of Constr 1999-03-29
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18152A2811999-10-12012 October 1999 Technical Basis for Elimination of Nozzle Inner Radius Insps (for Nozzles Other than Reactor Vessel),Technical Basis for ASME Section XI Code Case N-619 05000281/LER-1999-004-02, :on 981109,EDG Was Inoperable Longer than Allowed by TS Due to Governor Compensation Valve.Root Cause Evaluation Being Performed to Determine How Compensation Valve Became Closed1999-10-0101 October 1999
- on 981109,EDG Was Inoperable Longer than Allowed by TS Due to Governor Compensation Valve.Root Cause Evaluation Being Performed to Determine How Compensation Valve Became Closed
ML18152B3531999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Surry Power Station,Units 1 & 2.With ML18152B3371999-09-24024 September 1999 SER Accepting Third 10-year Interval Inservice Insp Plan Request for Relief SR-026 for Surry Power Station Unit 2 ML18152B6651999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Surry Power Station Units 1 & 2.With 05000280/LER-1999-006, :on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With1999-08-27027 August 1999
- on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With
05000280/LER-1999-005-01, :on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed1999-08-27027 August 1999
- on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed
ML18152B3841999-08-23023 August 1999 Safety Evaluation Granting Relief Request from ASME Section Xa Requirements for Containment Insp ML18152B3831999-08-23023 August 1999 Safety Evaluation Granting Relief Request from ASME Section XI Requirements for Containment Insp ML18152B3631999-08-23023 August 1999 Safety Evaluation Supporting Eddy Current Techniques Used by VEPCO to Determine Depth of Degradation Evident in Units SG Tubing & VEPCO Approach for Dispositioning Tubes with Avb Wear Indications ML18151A3981999-08-13013 August 1999 SPS Unit 2 ISI Summary Rept for 1999 Refueling Outage 05000280/LER-1999-004-01, :on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms1999-08-13013 August 1999
- on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms
ML18152B3791999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Surry Power Station,Units 1 & 2.With 05000281/LER-1999-003-02, :on 990705,auto Reactor Trip on Low Coolant Flow,Occurred.Caused by Loop Stop Valve Failure.Approved RCE Recommendations,Designed to Prevent Recurrence of Similar Event Will Be Implemented Through CAP1999-07-30030 July 1999
- on 990705,auto Reactor Trip on Low Coolant Flow,Occurred.Caused by Loop Stop Valve Failure.Approved RCE Recommendations,Designed to Prevent Recurrence of Similar Event Will Be Implemented Through CAP
ML20196J4781999-07-0101 July 1999 Safety Evaluation Supporting Amends 221 & 221 to Licenses DPR-32 & DPR-37,respectively ML18152B3911999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Surry Power Station,Units 1 & 2.With ML20195D3571999-06-0707 June 1999 Safety Evaluation Supporting Amends 220 & 220 to Licenses DPR-32 & DPR-37,respectively ML18152B4341999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Surry Power Station,Units 1 & 2.With ML20195E2401999-05-31031 May 1999 Rev 2 to COLR for SPS Unit 2 Cycle 16 Pattern Ag 05000281/LER-1999-002-02, :on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With1999-05-18018 May 1999
- on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With
ML18152B4161999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Surry Power Station Units 1 & 2.With 990512 Ltr 05000280/LER-1999-003-01, :on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With1999-04-28028 April 1999
- on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With
ML18152B6481999-04-14014 April 1999 Safety Evaluation Supporting Relief Requests IWE-2,4.5.6 & IWL-2 to Licenses DPR-32 & DPR-37 Respectively ML18152B6451999-04-13013 April 1999 SER Accepting Util Reactor Pressure Vessel Fluence Methodology for Surry Power Stations,Units 1 & 2 & North Anna Power Station,Units 1 & 2 Subject to Listed Limitations ML18152B6511999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Surry Power Station Units 1 & 2 05000281/LER-1999-001-02, :on 990301,RPS Relay Not Placed in Trip Resulted in Violation of TS 3.7.Caused by Lack of Procedural Guidance.Developed New Procedure to Provide More Explicit Instructions for Placing Stop Valve in Relay Trip1999-03-31031 March 1999
- on 990301,RPS Relay Not Placed in Trip Resulted in Violation of TS 3.7.Caused by Lack of Procedural Guidance.Developed New Procedure to Provide More Explicit Instructions for Placing Stop Valve in Relay Trip
05000280/LER-1999-002-01, :on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 9902121999-03-29029 March 1999
- on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212
ML18153A2741999-03-29029 March 1999 LER 99-002-00:on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212 05000280/LER-1998-013, :on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr1999-03-19019 March 1999
- on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr
ML20207L8081999-03-12012 March 1999 Safety Evaluation Supporting Amends 219 & 219 to Licenses DPR-32 & DPR-37 ML18152B7331999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Surry Power Station,Units 1 & 2.With ML18152B5381999-02-16016 February 1999 SER Accepting Third 10-year Interval Inservice Insp Request for Relief for Surry Power Station,Unit 1.Staff Concludes That Licensee Proposed Alternative Will Provide Acceptable Level of Quality & Safety.Technical Ltr Rept Also Encl ML18152B5421999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Surry Power Station,Units 1 & 2.With ML18151A3031999-01-29029 January 1999 ISI Summary Rept for 1998 Refueling Outage,Including Form NIS-1, Owners Rept for ISIs & Form NIS-2, Owners Rept for Repairs & Replacements 05000280/LER-1999-001, :on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable1999-01-21021 January 1999
- on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable
ML18152B6011998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Surry Power Station,Units 1 & 2.With ML18152B5861998-12-18018 December 1998 SER Approving Request Relief Related to Inservice Testing Program at Surry Power Station Unit 1 ML20198F9221998-12-16016 December 1998 Safety Evaluation Supporting Amends 217 & 217 to Licenses DPR-32 & DPR-37,respectively 05000280/LER-1998-014, :on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition1998-12-16016 December 1998
- on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition
ML18152B7121998-12-0404 December 1998 LER 98-S01-00:on 981105,noted Failure to Deactivate Station Access Badge.Caused by Human Error.Licensee Will Now Deactivate Station Badges Before Clearance Is Revoked & Process for Badge Deactivations Have Been Strengthened 05000280/LER-1998-012, :on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With1998-12-0101 December 1998
- on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With
ML18152B7081998-11-30030 November 1998 Rev 0 to COLR for Surry 1 Cycle 16,Pattern Un ML18152B5721998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Surry Power Station,Units 1 & 2.With ML18152B6241998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Surry Power Station Units 1 & 2.With ML18152B6881998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Surry Power Station Units 1 & 2.With ML20151U7261998-09-0303 September 1998 Safety Evaluation Approving Exemption from Certain 10CFR20 Requirements Re Use of self-contained Breathing Apparatus with Enriched Oxygen in Subatmospheric Containments at SPS ML18153A3271998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Surry Power Station,Units 1 & 2 ML20237E9721998-08-26026 August 1998 Safety Evaluation Supporting Amends 216 & 216 to Licenses DPR-32 & DPR-37,respectively ML18153A3161998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Surry Power Station Units 1 & 2 05000280/LER-1998-010, :on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status1998-07-31031 July 1998
- on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status
1999-09-30
[Table view] |
Text
POW 28-06-_01 NRC Form 366 * (9-83,) U.S. NUCLEAR REGULATORY COMMISSION APPROVED 0MB NO. 3160,0104 EXPIRES: 8/31/88 LICENSEE EVENT REPORT (LER) FACILITY NAME (1) !DOCKET NUMBER (2) PAGE 131
Unit 1 o I 5 I o Io I o 12 I 8 I O 1 loF O I 3 TITLE (41 Inadequate R*eview of AFW Suoply FollowinQ a HELB in Safecrnards EVENT DATE (5) LER NUMBER (6) REPORT DATE (71 OTHER FACILITIES INVOLVED (Bl MONTH DAY YEAR YEAR FACILITY NAMES DOCKET NUMBER(SI o I 6 31 o a 1 al 1 .:.... ol 1 14 -o I o ol 1
- 3 I o a I 1 01s1010101 I I OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check one or more of the folloV(inlJ)
(11) MODE (9) N 20.402(b) 20.406(cl 50,73(11(2)(ivl 73.71(bl -POWER 1
)(I) LEVEL -<101 1 I O I O 20.405t1H1Hm
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LICENSEE CONTACT FOR THIS LER (121 NAME TELEPHONE NUMBER AREA CODE D. L. Benson, Stat~n Manager . 81 01 4 31 51 7 I -I 31 11 8 Ill CAUSE SYSTEM COMPONENT I I I I I I I I COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (131 TURER I I I I I I SUP~LEMENTAL REPORT EXPECTED (141 SYSTEM I I COMPONENT.
I I I I I I . MANUFAC-TURER I I I I I I EXPECTED SUBMISSION MONTH DAY YEAR :1 YES /If v**. complete EXPECTED SUBMISSION DATE) DATE (151 nl1 ~11 RIR ABSTRACT (Limit to 1400 spaces, i.B., approximately fifteen single-space typewritten lines} (161 NRC Form 386 19-83) On June 30, 1987 with Unit One at 100% power and Unit Two at 69% power, *it was determined as a result of a company initiated
- safety system functional inspection, that a unique scenario could exist whereby auxiliary feedwater (AFW) {EIIS-BA}
could be lost to*an operating unit. In the event of a high energy line break (HELB) in the main steam valve house (MSVH) of an operating unit, the AFW pumps {EIIS-P} on that unit could be rendered inoperable due to the harsh environment.
With the unaffected unit at cold shutdown and only one of its motor driven AFW pumps available for cross connect to the affected unit, an assumed loss of offsite power, with a single failure could result in a loss of AFW to the affected unit. Administrative controls have been established to ensure that . when a unit is above 350 degrees/450 psig, two motor driven AFW pumps will be available from the other unit. Engineeririg is reviewing the original s~fety analysis for the HELB (loss of AFW) to assess the adequacy of the evaluation and determine if additional corrective actions are required.
97oso~o 00 1il i~~&eo PDR " PDR s . ...._\ t P*' p., ,
NRC Form 366A* (9-83) FACILITY NAME (11 POW 28-06~01 LICENSEE EVENT REPORT (LER) TEXT CONTINUATION*
U,S, NUCLEAR REGULATORY COMMISSION APPROVED 0MB NO. 3150--0104 EXPIRES: 8/31/88 DOCKET NUMBER (21 LER NUMBER (61 PAGE (31 ?Urry Power Station, Unit 1 o Is Io Io I o 12 1 a I o a 11 -o I 114 -o I o -o I 2 oF o 13 TEXT /ff tnOf9 _,,. i& n,quintd, usa additional NRC Farm 366A 's/ (171 . NRC FORM 366A (9-831 1. 0 Description of the Event* On June 30, 1987 with Unit One at 100% power and Unit Two at 69% power, it was determined as a result of a company initiated safety system functional inspection, that a unique scenario could exist whereby auxiliary feedwater
could be lost to an operating unit. In the event of a high energy line break (HELB) in the main steam valve house (MSVH) of an operating unit, the AFW pumps {EIIS-P} on that unit could be rendered inoperable due to the harsh environment.
With the unaffected unit at cold .shutdown and only one of its motor driven AFW pumps available.*
for cross connect to the affected unit, an assumed loss of offsite power, with a single failure could result in a loss of AFW to' the affected unit. The existing Technical Specification requires that only one motor driven AFW pump be available when the unit is at cold shutdown.
This specification was developed in 1980 to provide assurance that AFW could be supplied from one unit to another in the event that the AFW pumps in one unit were destroyed by fire (Appendix R). The HELB event was not considered at that time, and Appendix R does not require cqnsideration of the single failure criterion.
This event is reportable in accordance with lOCFR 50. 73(a) (2) (v). 2.0 Safety Consequences and Implications This scenario is not analyzed in the UFSAR. ever, a main steam line break is a condition IV event and is of very low probability.
Engineering is reviewing the original safety analysis to determine whether an unreviewed safety question exists. Additionally, Functional Restoration Procedure H.l provides guidance in-the event of total loss of FW and AFW to the Steam Generators.
Further protection is provided through an extensive non-destructive testing program of the main steam postulated break points in the main steam valve house .
NRC Form 366A 19-831 FACILITY NAME (1) e .pow 28-06-01 e .. LICENSEE EVENT REPORT (LERI TEXT CONTINUATION DOCKET NUMBER 121 U.S. NUCLEAR REGULATORY COMMISSION APPROVED 0MB NO. 3150-0104 EXPIRES: 8/31/88 PAGE 13) SURRY POWER STATION, UNIT 1 o 15 Io Io Io 12 I 810 81 7 -o 11 I 4 lo In n I ':l OF n h TEXT (If mo,e-,,.c.
ia ,wqund, u* tldditioMI NRC Form 366A'1/ l17l NRc FOAM 366.A 19-831 3.0 Cause Section l4B.5.1.7 of the UFSAR considers a HELB in the MSVH and assumes that should all three of the affected units AFW pumps become inoperable; redundancy is not lost because there are three AFW pumps* available from the unaffected unit. The UFSAR does not consider .the possibility that only one AFW pump from the unaffected unit might be available when that unit is at cold shutdown.
4.0 Immediate Corrective Action Administrative controls have been established to ensure that when a unit is above 350 degrees/450 psig, two motor driven AFW pumps will be available from the other unit. ,. 5.0 Additional Corrective Actions Engineering is reviewing the original safety analysis for the HELB (loss of AFW) to assess the adequacy of the evaluation and to qetermine if additional corrective actions are required.
6.0 Actions Taken to Prevent Recurrence None. 7.0 Similar Events None 8.0 Manufacturer/Model Number N/A
- U.S.GPO: 1986*0*824-538/455
.. e Vepco . July 30, 1987 U.S. Nuclear Regulatory Commission Document Control Desk 016 Phillips Building Washington, D.C. 20555 Gentlemen:
Pursuant to Surry Power Station Technical and Power Company hereby submits the for Surry Unit 1 and 2. VIRGINIA ELECTRIC AND POWER COMPANY P, D. Box 315 Surry, Virginia 23883 Serial No: 87-016 Docket No: 50-280 50-281 License No: DPR-32 DPR-37 Specifications~
Virginia Electric following Licensee Event Report REPORT NUMBER 87-014-00 This report has been reviewed by the Station Nuclear Safety and Operating Committee and will be reviewed by Safety Evaluation and Control. Very truly yours, David L. Benson Station Manager Enclosure pc: Dr. J. Nelson Grace Regional Administrator Suite 2900 101 Marietta Street, NW Atlanta, Georgia 30323