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POW 28-06-_01 NRC Form 366 *
(9-83,)
U.S. NUCLEAR REGULATORY COMMISSION APPROVED 0MB NO. 3160,0104 EXPIRES: 8/31/88 LICENSEE EVENT REPORT (LER)
FACILITY NAME (1)
DOCKET NUMBER (2)
PAGE 131
- Surry P9wer *station. Unit 1 o I 5 I o Io I o 12 I 8 I O 1 loF O I 3 TITLE (41 Inadequate R*eview of AFW Suoply FollowinQ a HELB in Safecrnards EVENT DATE (5)
LER NUMBER (6)
REPORT DATE (71 OTHER FACILITIES INVOLVED (Bl MONTH DAY YEAR YEAR FACILITY NAMES DOCKET NUMBER(SI o I 6 31 o a 1 al 1.:.... ol 1 14 - o I o ol 1
I OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check one or more of the folloV(inlJ) (11)
MODE (9)
N 20.402(b) 20.406(cl 50,73(11(2)(ivl 73.71(bl POWER 1
LEVEL
<101 1 I O I O 20.405t1H1Hm
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50.73(11(21(v) 73.71(cl 50.38(cl(2) 50.73(1)(2l{viil.
OTHER (Spacify in Abstr*ct bl/ow and in T*Kt, NRC Form
=~== :::::::::;:
60.73(11(21(11
&0.73(1)(2)(vllll(A) 366A) 50,73(11{2){ill 50.73(11(21(vllll(BI 50.73(11(2)(iiil 50.73(1)(21(,i)
LICENSEE CONTACT FOR THIS LER (121 NAME TELEPHONE NUMBER AREA CODE D. L. Benson, Stat~n Manager
. 81 01 4 31 51 7 I - I 31 11 8 Ill CAUSE SYSTEM COMPONENT I
I I
I I
I I I COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (131 MANUFAC-TURER I
I I
I I I SUP~LEMENTAL REPORT EXPECTED (141 SYSTEM I
I COMPONENT.
I I
I I I I.
MANUFAC-TURER I
I I
I I I EXPECTED SUBMISSION MONTH DAY YEAR
- 1 YES /If v**. complete EXPECTED SUBMISSION DATE)
DATE (151 nl1
~11 RIR ABSTRACT (Limit to 1400 spaces, i.B., approximately fifteen single-space typewritten lines} (161 NRC Form 386 19-83)
On June 30, 1987 with Unit One at 100% power and Unit Two at 69%
power, *it was determined as a result of a company initiated
- safety system functional inspection, that a unique scenario could exist whereby auxiliary feedwater (AFW) {EIIS-BA} could be lost to*an operating unit.
In the event of a high energy line break (HELB) in the main steam valve house (MSVH) of an operating unit, the AFW pumps {EIIS-P} on that unit could be rendered inoperable due to the harsh environment.
With the unaffected unit at cold shutdown and only one of its motor driven AFW pumps available for cross connect to the affected unit, an assumed loss of offsite power, with a single failure could result in a loss of AFW to the affected unit.
Administrative controls have been established to ensure that when a unit is above 350 degrees/450 psig, two motor driven AFW pumps will be available from the other unit.
Engineeririg is reviewing the original s~fety analysis for the HELB (loss of AFW) to assess the adequacy of the evaluation and determine if additional corrective actions are required.
97oso~o001il i~~&eo PDR PDR s
....._\\ t P*' p.,, (9-83)
FACILITY NAME (11 POW 28-06~01 LICENSEE EVENT REPORT (LER) TEXT CONTINUATION*
U,S, NUCLEAR REGULATORY COMMISSION APPROVED 0MB NO. 3150--0104 EXPIRES: 8/31/88 DOCKET NUMBER (21 LER NUMBER (61 PAGE (31
?Urry Power Station, Unit 1 o Is Io Io I o 12 1 a I o a 11 -
o I 114 -
o I o -o I 2 oF o 13 TEXT /ff tnOf9 _,,. i& n,quintd, usa additional NRC Farm 366A 's/ (171
. NRC FORM 366A (9-831
- 1. 0 Description of the Event*
On June 30, 1987 with Unit One at 100% power and Unit Two at 69% power, it was determined as a result of a company initiated safety system functional inspection, that a unique scenario could exist whereby auxiliary feedwater * (AFW) {EIIS.:..BA} could be lost to an operating unit.
In the event of a high energy line break (HELB) in the main steam valve house (MSVH) of an operating unit, the AFW pumps {EIIS-P} on that unit could be rendered inoperable due to the harsh environment.
With the unaffected unit at cold.shutdown and only one of its motor driven AFW pumps available.*
for cross connect to the affected unit, an assumed loss of offsite power, with a single failure could result in a loss of AFW to' the affected unit.
The existing Technical Specification requires that only one motor driven AFW pump be available when the unit is at cold shutdown.
This specification was developed in 1980 to provide assurance that AFW could be supplied from one unit to another in the event that the AFW pumps in one unit were destroyed by fire (Appendix R).
The HELB event was not considered at that time, and Appendix R does not require cqnsideration of the single failure criterion.
This event is reportable in accordance with 10CFR
- 50. 73(a) (2) (v).
2.0
Safety Consequences and Implications
This scenario is not analyzed in the UFSAR.
How-ever, a main steam line break is a condition IV event and is of very low probability.
Engineering is reviewing the original safety analysis to determine whether an unreviewed safety question exists.
Additionally, Functional Restoration Procedure H.l provides guidance in-the event of total loss of FW and AFW to the Steam Generators.
Further protection is provided through an extensive non-destructive testing program of the main steam postulated break points in the main steam valve house.19-831 FACILITY NAME (1) e
.pow 28-06-01 e..
LICENSEE EVENT REPORT (LERI TEXT CONTINUATION DOCKET NUMBER 121 U.S. NUCLEAR REGULATORY COMMISSION APPROVED 0MB NO. 3150-0104 EXPIRES: 8/31/88 PAGE 13)
SURRY POWER STATION, UNIT 1 o 15 Io Io Io 12 I 810 81 7 -
o 11 I 4 lo In n I ':l OF n h TEXT (If mo,e-,,.c. ia,wqund, u* tldditioMI NRC Form 366A'1/ l17l NRc FOAM 366.A 19-831 3.0
Cause
Section l4B.5.1.7 of the UFSAR considers a HELB in the MSVH and assumes that should all three of the affected units AFW pumps become inoperable; redundancy is not lost because there are three AFW pumps* available from the unaffected unit.
The UFSAR does not consider
.the possibility that only one AFW pump from the unaffected unit might be available when that unit is at cold shutdown.
4.0
Immediate Corrective Action
Administrative controls have been established to ensure that when a unit is above 350 degrees/450 psig, two motor driven AFW pumps will be available from the other unit.
5.0
Additional Corrective Actions
Engineering is reviewing the original safety analysis for the HELB (loss of AFW) to assess the adequacy of the evaluation and to qetermine if additional corrective actions are required.
6.0 Actions Taken to Prevent Recurrence None.
7.0
Similar Events
None 8.0 Manufacturer/Model Number N/A
- U.S.GPO: 1986*0*824-538/455
e Vepco
. July 30, 1987 U.S. Nuclear Regulatory Commission Document Control Desk 016 Phillips Building Washington, D.C.
20555 Gentlemen:
Pursuant to Surry Power Station Technical and Power Company hereby submits the for Surry Unit 1 and 2.
VIRGINIA ELECTRIC AND POWER COMPANY P, D. Box 315 Surry, Virginia 23883 Serial No:
87-016 Docket No:
50-280 50-281 License No: DPR-32 DPR-37 Specifications~ Virginia Electric following Licensee Event Report REPORT NUMBER 87-014-00 This report has been reviewed by the Station Nuclear Safety and Operating Committee and will be reviewed by Safety Evaluation and Control.
Very truly yours, David L. Benson Station Manager Enclosure pc:
Dr. J. Nelson Grace Regional Administrator Suite 2900 101 Marietta Street, NW Atlanta, Georgia 30323
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| 05000280/LER-1987-001, :on 861223,pressurizer PORVs Declared Inoperable Due to Excessive Stroke Time.Caused by Insufficient Air Flow Due to Air Line Size.Air Lines Will Be Replaced W/Larger Tubing |
- on 861223,pressurizer PORVs Declared Inoperable Due to Excessive Stroke Time.Caused by Insufficient Air Flow Due to Air Line Size.Air Lines Will Be Replaced W/Larger Tubing
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | | 05000281/LER-1987-001-03, :on 870312,loss of Reactor Coolant Loop Occurred Due to Loss of Charging Pumps & Seal Injection Flow to Reactor Cooling Pumps.Caused by Personnel Error.Personnel Reinstructed Re Listed Procedures |
- on 870312,loss of Reactor Coolant Loop Occurred Due to Loss of Charging Pumps & Seal Injection Flow to Reactor Cooling Pumps.Caused by Personnel Error.Personnel Reinstructed Re Listed Procedures
| | | 05000280/LER-1987-002-02, :on 870104,three Control/Relay Room Chillers Tripped on High Condenser Discharge Pressure.Caused by Insufficient Svc Water Flow to Condenser of Chiller Unit. Valve Lineup to & from Chiller Checked |
- on 870104,three Control/Relay Room Chillers Tripped on High Condenser Discharge Pressure.Caused by Insufficient Svc Water Flow to Condenser of Chiller Unit. Valve Lineup to & from Chiller Checked
| | | 05000281/LER-1987-002-01, :on 870316,reactor Trip by Turbine Trip Occurred,Resulting in Insertion of Shutdown Banks.Caused by Personnel Error.Reactor Trip Breakers Reset & Shutdown Banks Withdrawn |
- on 870316,reactor Trip by Turbine Trip Occurred,Resulting in Insertion of Shutdown Banks.Caused by Personnel Error.Reactor Trip Breakers Reset & Shutdown Banks Withdrawn
| | | 05000280/LER-1987-003, :on 870213 & 16,one of Three Control/Relay Room Chillers Operable.Second Chiller Out for Maint & Third Chiller Inoperable.Caused by Inadequate Heat Sinks.One Chiller Replaced,Two New Chillers Ordered |
- on 870213 & 16,one of Three Control/Relay Room Chillers Operable.Second Chiller Out for Maint & Third Chiller Inoperable.Caused by Inadequate Heat Sinks.One Chiller Replaced,Two New Chillers Ordered
| | | 05000281/LER-1987-003-01, :on 870404,reactor Tripped by Generator anti- Motoring Turbine Trip.Caused by Leaking Turbine Governor Valves.Valves Will Be Inspected & Repaired During Next Outage of Sufficient Duration |
- on 870404,reactor Tripped by Generator anti- Motoring Turbine Trip.Caused by Leaking Turbine Governor Valves.Valves Will Be Inspected & Repaired During Next Outage of Sufficient Duration
| | | 05000280/LER-1987-004, :on 870213,discovered Potential for Control Room Ventilation Fans to Admit More Unfiltered Air than Allowed.Caused by Inadequate Sealing of Fan Shaft.Temporary Seal Installed Until Fans Repaired |
- on 870213,discovered Potential for Control Room Ventilation Fans to Admit More Unfiltered Air than Allowed.Caused by Inadequate Sealing of Fan Shaft.Temporary Seal Installed Until Fans Repaired
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000281/LER-1987-004-03, :on 870831,while Performing Surveillance Procedure,Containment Cooling Water Outlet Header Isolation Trip Valve Found Inoperable.Caused by Ruptured Diaphragm in Air Pilot Relay.Relay Replaced |
- on 870831,while Performing Surveillance Procedure,Containment Cooling Water Outlet Header Isolation Trip Valve Found Inoperable.Caused by Ruptured Diaphragm in Air Pilot Relay.Relay Replaced
| | | 05000280/LER-1987-005, :on 870221,control/relay Room Chillers 1-VS-E-4B & 4C Tripped Due to Insufficient Svc Water Flow to Condensers.Caused by Clogged Y-type Suction Strainers. Maint Procedures Re Strainer Cleaning Revised |
- on 870221,control/relay Room Chillers 1-VS-E-4B & 4C Tripped Due to Insufficient Svc Water Flow to Condensers.Caused by Clogged Y-type Suction Strainers. Maint Procedures Re Strainer Cleaning Revised
| | | 05000281/LER-1987-005-03, :on 871014 Electrician Inadvertently Completed Flood Protection Circuit Causing Two of Four Condenser Circulating Water Inlet Valves to Close.Caused by Personnel Error.Procedure Written for Maint Personnel |
- on 871014 Electrician Inadvertently Completed Flood Protection Circuit Causing Two of Four Condenser Circulating Water Inlet Valves to Close.Caused by Personnel Error.Procedure Written for Maint Personnel
| | | 05000280/LER-1987-006, :on 870310,control/relay Chiller Observed Inoperable Due to Chiller Svc Water Pump Trip.Cause of Pump Trip Not Determined.Thermal Trip Device Reset |
- on 870310,control/relay Chiller Observed Inoperable Due to Chiller Svc Water Pump Trip.Cause of Pump Trip Not Determined.Thermal Trip Device Reset
| | | 05000280/LER-1987-007, :on 870323,one (1-VS-E-4A) of Three Control/ Relay Room Chillers (EIIS-CHU) Tripped.Caused by Insufficient Svc Water Flow Due to Seal Leak on Supply Pump.Svc Water Flow Increased & Pump Repaired |
- on 870323,one (1-VS-E-4A) of Three Control/ Relay Room Chillers (EIIS-CHU) Tripped.Caused by Insufficient Svc Water Flow Due to Seal Leak on Supply Pump.Svc Water Flow Increased & Pump Repaired
| | | 05000280/LER-1987-008, :on 870326,one of Three Control/Relay Room Chillers Tripped Due to High Condenser Discharge Pressure. Caused by Operator Error.Addl Valve Handles Will Be Installed on Each Chiller |
- on 870326,one of Three Control/Relay Room Chillers Tripped Due to High Condenser Discharge Pressure. Caused by Operator Error.Addl Valve Handles Will Be Installed on Each Chiller
| | | 05000280/LER-1987-009-02, :on 870330,discovered That Inside Containment Isolation Valve for Containment Sump Pumps Would Not Close. Caused by Corrosion Product Buildup in Valve Operator.New Valve Operator Installed |
- on 870330,discovered That Inside Containment Isolation Valve for Containment Sump Pumps Would Not Close. Caused by Corrosion Product Buildup in Valve Operator.New Valve Operator Installed
| | | 05000280/LER-1987-010, :on 870313,improper Routing of App B Related Cables Discovered.Caused by Relocation of Cables Through Cable Vault & Tunnel.Fire Watch of Area at Least Once Per Shift Established & Design Changes Reviewed |
- on 870313,improper Routing of App B Related Cables Discovered.Caused by Relocation of Cables Through Cable Vault & Tunnel.Fire Watch of Area at Least Once Per Shift Established & Design Changes Reviewed
| | | 05000280/LER-1987-011, :on 870516,low Flow RCS (EIIS-AB) Flow Reduced to 47%,following Reactor Trip.Caused by Failure of RCS a Hot Leg Loop Stop Valve.Samples of Loop Stop Valve Stems Will Undergo Ultrasonic Testing |
- on 870516,low Flow RCS (EIIS-AB) Flow Reduced to 47%,following Reactor Trip.Caused by Failure of RCS a Hot Leg Loop Stop Valve.Samples of Loop Stop Valve Stems Will Undergo Ultrasonic Testing
| | | 05000280/LER-1987-011-01, :on 870516,low Flow Reactor Trip Occurred. Caused by Hot Leg Loop Stop Valve Stem Failure Permitting Disc to Drop,Blocking Loop Flow.Procedure Revised to Reduce Stress on Valve Stem |
- on 870516,low Flow Reactor Trip Occurred. Caused by Hot Leg Loop Stop Valve Stem Failure Permitting Disc to Drop,Blocking Loop Flow.Procedure Revised to Reduce Stress on Valve Stem
| | | 05000280/LER-1987-012-01, :on 870607,recirculation Spray Pump Declared Inoperable Due to High Vibrations.Caused by Threaded Nut & Bolt Detached & Located in Impeller Region of Pump.Loose Nut & Bolt Removed & Pump Realigned |
- on 870607,recirculation Spray Pump Declared Inoperable Due to High Vibrations.Caused by Threaded Nut & Bolt Detached & Located in Impeller Region of Pump.Loose Nut & Bolt Removed & Pump Realigned
| | | 05000280/LER-1987-013-01, :on 870623,unit Shutdown Commenced Due to High RCS Leak Rate.Caused by Failed Packing on Loop Stop Valve MOV-1593.Loop Stop Valves Repacked & Diaphragm on Drain Header Isolation Valve Replaced |
- on 870623,unit Shutdown Commenced Due to High RCS Leak Rate.Caused by Failed Packing on Loop Stop Valve MOV-1593.Loop Stop Valves Repacked & Diaphragm on Drain Header Isolation Valve Replaced
| | | 05000280/LER-1987-014, :on 870630,discovered That Auxiliary Feedwater (AFW) Could Be Lost to Operating Unit in Event of High Energy Line Break in Main Steam Valve House.Caused by Poor Review of AFW Supply.Review Continuing |
- on 870630,discovered That Auxiliary Feedwater (AFW) Could Be Lost to Operating Unit in Event of High Energy Line Break in Main Steam Valve House.Caused by Poor Review of AFW Supply.Review Continuing
| | | 05000280/LER-1987-015-01, :on 870717,individual Rod Position Indicators for Shutdown Banks a & B & Control Banks A,B,C & D Declared Inoperable.Caused by Banks Indicating Below Demand Counter Position Due to Dirty Dc Power Contacts |
- on 870717,individual Rod Position Indicators for Shutdown Banks a & B & Control Banks A,B,C & D Declared Inoperable.Caused by Banks Indicating Below Demand Counter Position Due to Dirty Dc Power Contacts
| | | 05000280/LER-1987-016, :on 870722,main Control Ventilation Isolation Occurred.Caused by High Sensor Voltage on Chlorine Gas Detector.Chlorine Gas Treatment Sys & Sewage Treatment Plant Replaced by Ultraviolet Sys |
- on 870722,main Control Ventilation Isolation Occurred.Caused by High Sensor Voltage on Chlorine Gas Detector.Chlorine Gas Treatment Sys & Sewage Treatment Plant Replaced by Ultraviolet Sys
| | | 05000280/LER-1987-017-01, :on 870727,containment Vacuum Flow Paths for Units 1 & 2 Became Inoperable When Discharge Valves Closed. Caused by Electrical Spiking Due to Failed Central Processing Unit Card.Failed Card Replaced |
- on 870727,containment Vacuum Flow Paths for Units 1 & 2 Became Inoperable When Discharge Valves Closed. Caused by Electrical Spiking Due to Failed Central Processing Unit Card.Failed Card Replaced
| | | 05000280/LER-1987-018, :on 870729,control/relay Room Chiller a Freon Relief Valve Lifted.Chillers B & C Tripped on Listed Dates. Caused by Low Svc Water (SW) Flow Due to Buildup of Seaweed in Upstream SW Strainers.Strainers Cleared |
- on 870729,control/relay Room Chiller a Freon Relief Valve Lifted.Chillers B & C Tripped on Listed Dates. Caused by Low Svc Water (SW) Flow Due to Buildup of Seaweed in Upstream SW Strainers.Strainers Cleared
| | | 05000280/LER-1987-019, :on 870807,manual Reactor Trip Initiated Following Short Rampdown Due to Loss of Cooling & Oil Flow for Main Transformer B.Caused by Failed Undervoltage Relay. Relay & Local Annunciator Panel Replaced |
- on 870807,manual Reactor Trip Initiated Following Short Rampdown Due to Loss of Cooling & Oil Flow for Main Transformer B.Caused by Failed Undervoltage Relay. Relay & Local Annunciator Panel Replaced
| | | 05000280/LER-1987-020, :on 870813 & 21,main Control Room Ventilation Isolated.Caused by High Voltage Output on Chlorine Gas Detector CLA-VS-100A.Ventilation Sys Realigned & Verified No Chlorine Gas in Room |
- on 870813 & 21,main Control Room Ventilation Isolated.Caused by High Voltage Output on Chlorine Gas Detector CLA-VS-100A.Ventilation Sys Realigned & Verified No Chlorine Gas in Room
| | | 05000280/LER-1987-021, :on 870818,control/relay Room Chiller 1-VS-E-4B Tripped on High Condenser Discharge Pressure.Caused by Inadequate Svc Water Flow Due to Buildup of Seaweed in Y-type Suction Strainers.Strainers Cleaned |
- on 870818,control/relay Room Chiller 1-VS-E-4B Tripped on High Condenser Discharge Pressure.Caused by Inadequate Svc Water Flow Due to Buildup of Seaweed in Y-type Suction Strainers.Strainers Cleaned
| | | 05000280/LER-1987-022, :on 870830 & 0903,main Control Room Ventilation Isolation Occurred.Caused by High Voltage Output on Chlorine Gas Detector.Chemistry Dept Verified That No Chlorine in Main Control Room.Ventilation Sys Realigned |
- on 870830 & 0903,main Control Room Ventilation Isolation Occurred.Caused by High Voltage Output on Chlorine Gas Detector.Chemistry Dept Verified That No Chlorine in Main Control Room.Ventilation Sys Realigned
| | | 05000280/LER-1987-023, :on 870901,standby Charging Pump Automatically Started on Low Charging Pump Discharge Pressure Signal. Caused by Personnel Error.Pressure Transmitter Drain Valve Closed & Isolation Valve Opened |
- on 870901,standby Charging Pump Automatically Started on Low Charging Pump Discharge Pressure Signal. Caused by Personnel Error.Pressure Transmitter Drain Valve Closed & Isolation Valve Opened
| 10 CFR 50.73(o)(2) | | 05000280/LER-1987-024, :on 870920,RCS Flow Reactor Trip Occurred When Reactor Coolant Pump B Tripped.Caused by Complete Separation of Phase Main Load Connection Bus Bar A.Failed Bus Bar Replaced & Other Bus Bars Inspected |
- on 870920,RCS Flow Reactor Trip Occurred When Reactor Coolant Pump B Tripped.Caused by Complete Separation of Phase Main Load Connection Bus Bar A.Failed Bus Bar Replaced & Other Bus Bars Inspected
| | | 05000280/LER-1987-025, :on 871008,RCS Leakage Rate Test Results of 4.06 Gpm Found in Excess of Tech Specs 3.1.C.2 & 3.1.C.5. Caused by Inadequate Procedure & HX Bypass Valve Leakage. Valve Tightened & Procedure PT-10 Revised |
- on 871008,RCS Leakage Rate Test Results of 4.06 Gpm Found in Excess of Tech Specs 3.1.C.2 & 3.1.C.5. Caused by Inadequate Procedure & HX Bypass Valve Leakage. Valve Tightened & Procedure PT-10 Revised
| | | 05000280/LER-1987-026, :on 871018,main Control Room (MCR) Ventilation Isolated Due to High Voltage Output on Chlorine Gas Detector.Chemistry Verified No Chlorine Gas in MCR & Ventilation Sys Realigned |
- on 871018,main Control Room (MCR) Ventilation Isolated Due to High Voltage Output on Chlorine Gas Detector.Chemistry Verified No Chlorine Gas in MCR & Ventilation Sys Realigned
| | | 05000280/LER-1987-027, :on 871027,electrical Short in Train a Turbine Bldg Flood Control Panel Caused Spurious Completion of Flood Protection Circuit.Caused by Leak on Access Manway of Moisture Separator Reheater 1-MS-E-1B |
- on 871027,electrical Short in Train a Turbine Bldg Flood Control Panel Caused Spurious Completion of Flood Protection Circuit.Caused by Leak on Access Manway of Moisture Separator Reheater 1-MS-E-1B
| | | 05000280/LER-1987-028, :on 871021,reported That Emergency Diesel Generators Output Breaker Protection Circuits Contained Instantaneous Overcurrent Tripping Relays.Caused by Design Deficiency.Trip Relay Settings Increased |
- on 871021,reported That Emergency Diesel Generators Output Breaker Protection Circuits Contained Instantaneous Overcurrent Tripping Relays.Caused by Design Deficiency.Trip Relay Settings Increased
| | | 05000280/LER-1987-029, :on 871108,main Control Room Ventilation Isolated Due to High Voltage Output on Chlorine Detector. Caused by Increased Voltage Output Inducing Spurious Signal.Ventilation Sys Realigned |
- on 871108,main Control Room Ventilation Isolated Due to High Voltage Output on Chlorine Detector. Caused by Increased Voltage Output Inducing Spurious Signal.Ventilation Sys Realigned
| | | 05000280/LER-1987-031, :on 871112,containment Isolation Valve Observed to Be Inoperable.Caused by Mechanical Binding of Valve Operator.Valve Operator Freed.Insp Performed on Similar Valves.Engineering Work Request Initiated |
- on 871112,containment Isolation Valve Observed to Be Inoperable.Caused by Mechanical Binding of Valve Operator.Valve Operator Freed.Insp Performed on Similar Valves.Engineering Work Request Initiated
| | | 05000280/LER-1987-032, :on 871111,RCS (EIIS AB) Loop B Average Temp Protection Channel Failed High.Caused by Power Supply Failure of Summator in Signal Conditioning Circuitry. Summator Hagan/4111084-003 Replaced |
- on 871111,RCS (EIIS AB) Loop B Average Temp Protection Channel Failed High.Caused by Power Supply Failure of Summator in Signal Conditioning Circuitry. Summator Hagan/4111084-003 Replaced
| 10 CFR 50.73(a)(2) | | 05000280/LER-1987-033, .On 871124,charging Pump Component Cooling Water Sys (EIIS-CC) Became Inoperable.Caused by Inadequate Hydrostatic Test Procedure.Procedure Enhancement to Include Sys Depressurizing Instructions Planned | .On 871124,charging Pump Component Cooling Water Sys (EIIS-CC) Became Inoperable.Caused by Inadequate Hydrostatic Test Procedure.Procedure Enhancement to Include Sys Depressurizing Instructions Planned | | | 05000280/LER-1987-034, :on 871126,specific Activity Sample of Reactor Coolant Showed Dose Equivalent I-131 of 1.19 Uci/Cc.Caused by Fuel Element Defect in Reactor Core.Required Tech Spec 4.1.2B Implemented |
- on 871126,specific Activity Sample of Reactor Coolant Showed Dose Equivalent I-131 of 1.19 Uci/Cc.Caused by Fuel Element Defect in Reactor Core.Required Tech Spec 4.1.2B Implemented
| 10 CFR 50.73(a)(2) 10 CFR 50.73(o)(2)(vii) | | 05000280/LER-1987-035, :on 870717,emergency Diesel Generator Degraded/ Undervoltage Protection Surveillance Not Performed.Caused by Failure to Incorporate Tech Spec Amend Into Test Program. Special Tests of Interlocks Performed |
- on 870717,emergency Diesel Generator Degraded/ Undervoltage Protection Surveillance Not Performed.Caused by Failure to Incorporate Tech Spec Amend Into Test Program. Special Tests of Interlocks Performed
| | | 05000280/LER-1987-036, :on 871202,during Hot Shutdown Inner Door of Containment Personnel Air Lock Exceeded Leakage Criteria for Periodic Test 16.7.Caused by Inadequate Seal.Shim Welded to Actuator Mechanism to Allow Proper Sealing |
- on 871202,during Hot Shutdown Inner Door of Containment Personnel Air Lock Exceeded Leakage Criteria for Periodic Test 16.7.Caused by Inadequate Seal.Shim Welded to Actuator Mechanism to Allow Proper Sealing
| | | 05000280/LER-1987-037, :on 871203,emergency Diesel Generator 3 Automatically Started.Caused by Blown Fuse & Failed Relay. Undervoltage Relay 59 ABC-1J1 & Dc Control Fuse Replaced.W/ |
- on 871203,emergency Diesel Generator 3 Automatically Started.Caused by Blown Fuse & Failed Relay. Undervoltage Relay 59 ABC-1J1 & Dc Control Fuse Replaced.W/
| | | 05000280/LER-1987-038, :on 871208,calculated Offsite Thyroid Dose from Steam Generator Tube Rupture Increased Due to Potential post-trip Steam Generator Tube Bundle Uncovery.Caused by Reanalysis Using Updated FSAR Assumptions |
- on 871208,calculated Offsite Thyroid Dose from Steam Generator Tube Rupture Increased Due to Potential post-trip Steam Generator Tube Bundle Uncovery.Caused by Reanalysis Using Updated FSAR Assumptions
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000280/LER-1987-039, :on 871215,protection Sys Channel Inoperable Due to Failed Summator in Signal Conditioning Circuit.Caused by Loss of Power to Summator.Affected Protection Channels & Summator Replaced & Returned to Normal |
- on 871215,protection Sys Channel Inoperable Due to Failed Summator in Signal Conditioning Circuit.Caused by Loss of Power to Summator.Affected Protection Channels & Summator Replaced & Returned to Normal
| | | 05000280/LER-1987-040, :on 871231,discovered That Containment Hog Particulate Filters Unintentionally Discarded.Caused by Failure to Perform Sr-89 & Sr-90 Analyses.Personnel Reinstructed in Procedures |
- on 871231,discovered That Containment Hog Particulate Filters Unintentionally Discarded.Caused by Failure to Perform Sr-89 & Sr-90 Analyses.Personnel Reinstructed in Procedures
| 10 CFR 50.73(a)(2)(i) |
|