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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000281/LER-1999-004-02, :on 981109,EDG Was Inoperable Longer than Allowed by TS Due to Governor Compensation Valve.Root Cause Evaluation Being Performed to Determine How Compensation Valve Became Closed1999-10-0101 October 1999
- on 981109,EDG Was Inoperable Longer than Allowed by TS Due to Governor Compensation Valve.Root Cause Evaluation Being Performed to Determine How Compensation Valve Became Closed
05000280/LER-1999-006, :on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With1999-08-27027 August 1999
- on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With
05000280/LER-1999-005-01, :on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed1999-08-27027 August 1999
- on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed
05000280/LER-1999-004-01, :on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms1999-08-13013 August 1999
- on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms
05000281/LER-1999-003-02, :on 990705,auto Reactor Trip on Low Coolant Flow,Occurred.Caused by Loop Stop Valve Failure.Approved RCE Recommendations,Designed to Prevent Recurrence of Similar Event Will Be Implemented Through CAP1999-07-30030 July 1999
- on 990705,auto Reactor Trip on Low Coolant Flow,Occurred.Caused by Loop Stop Valve Failure.Approved RCE Recommendations,Designed to Prevent Recurrence of Similar Event Will Be Implemented Through CAP
05000281/LER-1999-002-02, :on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With1999-05-18018 May 1999
- on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With
05000280/LER-1999-003-01, :on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With1999-04-28028 April 1999
- on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With
05000281/LER-1999-001-02, :on 990301,RPS Relay Not Placed in Trip Resulted in Violation of TS 3.7.Caused by Lack of Procedural Guidance.Developed New Procedure to Provide More Explicit Instructions for Placing Stop Valve in Relay Trip1999-03-31031 March 1999
- on 990301,RPS Relay Not Placed in Trip Resulted in Violation of TS 3.7.Caused by Lack of Procedural Guidance.Developed New Procedure to Provide More Explicit Instructions for Placing Stop Valve in Relay Trip
05000280/LER-1999-002-01, :on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 9902121999-03-29029 March 1999
- on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212
05000280/LER-1998-013, :on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr1999-03-19019 March 1999
- on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr
05000280/LER-1999-001, :on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable1999-01-21021 January 1999
- on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable
05000280/LER-1998-014, :on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition1998-12-16016 December 1998
- on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition
ML18152B7121998-12-0404 December 1998 LER 98-S01-00:on 981105,noted Failure to Deactivate Station Access Badge.Caused by Human Error.Licensee Will Now Deactivate Station Badges Before Clearance Is Revoked & Process for Badge Deactivations Have Been Strengthened 05000280/LER-1998-012, :on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With1998-12-0101 December 1998
- on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With
05000280/LER-1998-010, :on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status1998-07-31031 July 1998
- on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status
05000280/LER-1998-009, :on 980509,nonisolable Leak of Reactor Coolant Pump Seal Injection Line Weld,Was Discovered.Caused by Lack of Fusion or Thermal Fatigue Coupled W/Vibration Stress Due to Loose Rod Hanger.Rcp Seal Injection Line Removed1998-06-0303 June 1998
- on 980509,nonisolable Leak of Reactor Coolant Pump Seal Injection Line Weld,Was Discovered.Caused by Lack of Fusion or Thermal Fatigue Coupled W/Vibration Stress Due to Loose Rod Hanger.Rcp Seal Injection Line Removed
05000280/LER-1998-008, :on 980228,auxiliary Ventilation Fans Were Noted in Condition Outside of Design Basis.Caused by Failure to Recognize Potential Impact of Certain Design Basis Accident Scenarios.No Corrective Actions Needed1998-05-22022 May 1998
- on 980228,auxiliary Ventilation Fans Were Noted in Condition Outside of Design Basis.Caused by Failure to Recognize Potential Impact of Certain Design Basis Accident Scenarios.No Corrective Actions Needed
05000280/LER-1998-007, :on 980330,radiation Monitors Were Declared Inoperable.Caused by Change in Operating Temperature Range. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-61998-04-29029 April 1998
- on 980330,radiation Monitors Were Declared Inoperable.Caused by Change in Operating Temperature Range. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-6
05000280/LER-1998-006, :on 980324,unisolable Through Wall Leak of RCP Thermowell Was Noted.Cause of Leak Is Unknown.Rtd Will Be Replaced1998-04-22022 April 1998
- on 980324,unisolable Through Wall Leak of RCP Thermowell Was Noted.Cause of Leak Is Unknown.Rtd Will Be Replaced
05000280/LER-1998-005, :on 980212,fire Watch Insp Exceeded One Hour. Caused by Lack of Attention to Detail by Individual Involved.Individual Involved Was Coached on Requirement to Perform Fire Watch Patrols within Required Time Frame1998-04-22022 April 1998
- on 980212,fire Watch Insp Exceeded One Hour. Caused by Lack of Attention to Detail by Individual Involved.Individual Involved Was Coached on Requirement to Perform Fire Watch Patrols within Required Time Frame
05000280/LER-1998-003, :on 980226,no Procedural Guidance for Maintaining EDG Minimum Fuel Supply During Loop,Was Identified.Caused by Absence of Procedural Instructions. Deviation Rept Submitted to Document Deviating Condition1998-03-0909 March 1998
- on 980226,no Procedural Guidance for Maintaining EDG Minimum Fuel Supply During Loop,Was Identified.Caused by Absence of Procedural Instructions. Deviation Rept Submitted to Document Deviating Condition
05000280/LER-1998-004, :on 980206,fire Watch Was Released Prematurely Resulting in Violation of Ts.Caused by Inadequate Planning of Repair Activity.Work Orders Will Include Ref to Applicable Procedures Developed to Assist in Repairs1998-03-0606 March 1998
- on 980206,fire Watch Was Released Prematurely Resulting in Violation of Ts.Caused by Inadequate Planning of Repair Activity.Work Orders Will Include Ref to Applicable Procedures Developed to Assist in Repairs
05000280/LER-1998-002, :on 980202,automatic Turbine Trip Resulted in Automatic Reactor Trip.Caused Degraded Generator Voltage Regulator sub-component Failure.Placed Plant in Safe Hot SD & Replaced Intermittent Relay & Relay Socket1998-03-0404 March 1998
- on 980202,automatic Turbine Trip Resulted in Automatic Reactor Trip.Caused Degraded Generator Voltage Regulator sub-component Failure.Placed Plant in Safe Hot SD & Replaced Intermittent Relay & Relay Socket
05000280/LER-1998-001-01, :on 980108,deficient Test Due to Faulty Test Equipment Resulted in TS Violation.Caused by Faulty Vibration Analyzer Cable or Loose Connection.Station Deviation Rept Was Submitted1998-02-0606 February 1998
- on 980108,deficient Test Due to Faulty Test Equipment Resulted in TS Violation.Caused by Faulty Vibration Analyzer Cable or Loose Connection.Station Deviation Rept Was Submitted
05000280/LER-1997-009, :on 971014,declared Intake Canal Level Probes Inoperable Due to Marine Growth.Caused by Inadequate Maint of Intake Canal Level Probes.Subject Probes Were Cleaned, Tested Satisfactorily & Returned to Operable Status1998-01-13013 January 1998
- on 971014,declared Intake Canal Level Probes Inoperable Due to Marine Growth.Caused by Inadequate Maint of Intake Canal Level Probes.Subject Probes Were Cleaned, Tested Satisfactorily & Returned to Operable Status
05000280/LER-1997-012, :on 971028,loss of Power to Latching Mechanism on Several Doors Occurred.Caused by Tripping of Two Breakers in Security Distribution Panel.Reset Affected Breakers Which Restored Power to Security Systems & Affected Doors1998-01-13013 January 1998
- on 971028,loss of Power to Latching Mechanism on Several Doors Occurred.Caused by Tripping of Two Breakers in Security Distribution Panel.Reset Affected Breakers Which Restored Power to Security Systems & Affected Doors
05000281/LER-1997-004-02, :on 971202,invalid Mstv Indication Results in Manual Reactor Trip W/Esf Actuation Were Noted.Caused by Displaced Open Limit Switch Arms.Open Limit Switch for Mstv a Was Relocated Closer to Valve Position Bar1997-12-31031 December 1997
- on 971202,invalid Mstv Indication Results in Manual Reactor Trip W/Esf Actuation Were Noted.Caused by Displaced Open Limit Switch Arms.Open Limit Switch for Mstv a Was Relocated Closer to Valve Position Bar
05000281/LER-1997-002-01, :on 970713,main Steam High Range Radiation Monitor Was Declared Inoperable.Caused by Equipment Failure. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-61997-12-10010 December 1997
- on 970713,main Steam High Range Radiation Monitor Was Declared Inoperable.Caused by Equipment Failure. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-6
05000280/LER-1997-011, :on 971030,determined That Periodic Test Procedures for Testing Reactor Trip Bypass Breakers Did Not Test Manual Undervoltage Trip.Caused by mis-interpretation of Term in-service. Procedures Revised1997-11-26026 November 1997
- on 971030,determined That Periodic Test Procedures for Testing Reactor Trip Bypass Breakers Did Not Test Manual Undervoltage Trip.Caused by mis-interpretation of Term in-service. Procedures Revised
05000280/LER-1997-010, :on 971028,discovered Missed Fire Protection Surveillance Pt.Caused by Personnel Error.Satisfactorily Completed PT Procedure 0-OPT-FP-009 & Diesel Driven Fire Pump 1-FP-P-2 Declared Operable1997-11-25025 November 1997
- on 971028,discovered Missed Fire Protection Surveillance Pt.Caused by Personnel Error.Satisfactorily Completed PT Procedure 0-OPT-FP-009 & Diesel Driven Fire Pump 1-FP-P-2 Declared Operable
05000281/LER-1997-003-02, :on 971014,Unit 2 MSSVs Revealed That Lift Setting for Two MSSVs Were Outside as Found Setpoint Tolerance.Caused by Minor Setpoint Drift.Repaired,Revised & Adjusted Safety Valves1997-11-13013 November 1997
- on 971014,Unit 2 MSSVs Revealed That Lift Setting for Two MSSVs Were Outside as Found Setpoint Tolerance.Caused by Minor Setpoint Drift.Repaired,Revised & Adjusted Safety Valves
05000280/LER-1997-008-01, :on 971011,invalid Actuation of ESF Occurred. Caused by Personnel Errors.Main CR Bottled Air Sys Isolated & Containment Hydrogen Analyzer Heat Tracing Actuation Signal Reset1997-11-0707 November 1997
- on 971011,invalid Actuation of ESF Occurred. Caused by Personnel Errors.Main CR Bottled Air Sys Isolated & Containment Hydrogen Analyzer Heat Tracing Actuation Signal Reset
05000280/LER-1997-007-01, :on 970930,determined That Plant Was Outside App R Design Basis Due to Vital Bus Isolation Issue.Caused by Personnel Error.Installed Circuit Protective Device During Oct 1997 Refueling Outage1997-10-30030 October 1997
- on 970930,determined That Plant Was Outside App R Design Basis Due to Vital Bus Isolation Issue.Caused by Personnel Error.Installed Circuit Protective Device During Oct 1997 Refueling Outage
05000281/LER-1997-002-03, :on 970713,CR annunciator,2-RMA-A-7 for Main Steam Line Effluent High Range Radiation Monitors Alarmed. Caused by Intermittent Component Failure.Preplanned Alternate Method of Monitoring Initiated1997-08-12012 August 1997
- on 970713,CR annunciator,2-RMA-A-7 for Main Steam Line Effluent High Range Radiation Monitors Alarmed. Caused by Intermittent Component Failure.Preplanned Alternate Method of Monitoring Initiated
05000280/LER-1997-001, :on 970123,shutdown Occurred Due to Drain Line Weld Leak.Inspected & Tested Turbine Trip Actuation Circuitry1997-06-10010 June 1997
- on 970123,shutdown Occurred Due to Drain Line Weld Leak.Inspected & Tested Turbine Trip Actuation Circuitry
05000280/LER-1997-005, :on 970502,Unit 1 Power Range Nuclear Instrumentation Was Inoperable Due to Personnel Error.Sro & STA That Were Involved in Event Were Counseled1997-05-28028 May 1997
- on 970502,Unit 1 Power Range Nuclear Instrumentation Was Inoperable Due to Personnel Error.Sro & STA That Were Involved in Event Were Counseled
05000280/LER-1997-006, :on 970320,loss of Refueling Integrity Due to Inadequate Containment Closure Process & Verification.Fuel Movement Stopped IAW Action Statement Requirements of TS 3.10.B1997-04-18018 April 1997
- on 970320,loss of Refueling Integrity Due to Inadequate Containment Closure Process & Verification.Fuel Movement Stopped IAW Action Statement Requirements of TS 3.10.B
05000280/LER-1997-004, :on 970317,main Steam Safety Valve Was Outside as Found Setpoint Tolerance.Specific Cause Unknown,However, Minor Setpoint Drift Can Be Expected.No Immediate Corrective Actions Performed1997-04-15015 April 1997
- on 970317,main Steam Safety Valve Was Outside as Found Setpoint Tolerance.Specific Cause Unknown,However, Minor Setpoint Drift Can Be Expected.No Immediate Corrective Actions Performed
05000280/LER-1997-002, :on 970116,one Train of Auxiliary Ventilation Sys Was Inoperable Outside of Ts.Caused by Personnel Error. Submitted Deviation Rept Re Reverse Rotation of Fan & Work Request to Adjust Linkage1997-04-0808 April 1997
- on 970116,one Train of Auxiliary Ventilation Sys Was Inoperable Outside of Ts.Caused by Personnel Error. Submitted Deviation Rept Re Reverse Rotation of Fan & Work Request to Adjust Linkage
05000281/LER-1997-001-01, :on 970218,manual Reactor Trip & ESF Actuation Occurred Due to Loss of EHC Control Power.Caused by Momentary Short.Relay Card Was Replaced1997-03-19019 March 1997
- on 970218,manual Reactor Trip & ESF Actuation Occurred Due to Loss of EHC Control Power.Caused by Momentary Short.Relay Card Was Replaced
05000280/LER-1997-003, :on 970219,loss of Pressurizer Heaters Resulted in Manual U1 Trip & U2 ESF Actuation.Caused by Loss of Group C Pressurizer Proportional Heaters.Reactor Trip Breakers Were Verified Open1997-03-19019 March 1997
- on 970219,loss of Pressurizer Heaters Resulted in Manual U1 Trip & U2 ESF Actuation.Caused by Loss of Group C Pressurizer Proportional Heaters.Reactor Trip Breakers Were Verified Open
05000280/LER-1997-002-01, :on 970116,one Train of Auxiliary Ventilation Sys Declared Inoperable.Caused by Personnel Error.Properly Adjusted Damper 1-VS-MOD-58B & Exited Seven Day LCO on 9701161997-02-13013 February 1997
- on 970116,one Train of Auxiliary Ventilation Sys Declared Inoperable.Caused by Personnel Error.Properly Adjusted Damper 1-VS-MOD-58B & Exited Seven Day LCO on 970116
05000281/LER-1997-002, :on 961213,automatic Reactor Trip Occurred During Planned Shutdown.Caused by Steam Flow/Feedwater Flow Mismatch.Rps Functioned as Designed & Plant Placed in Hot Shutdown1997-01-0202 January 1997
- on 961213,automatic Reactor Trip Occurred During Planned Shutdown.Caused by Steam Flow/Feedwater Flow Mismatch.Rps Functioned as Designed & Plant Placed in Hot Shutdown
05000280/LER-1996-008-01, :on 961112,water Gas Decay Tank Oxygen Analyzer Pressure Sensors Inoperable Due to Vendor Supplied Equipment Not Meeting Procurement specifications.Post-implementation Procedures Revised & Transducers Replaced1996-12-12012 December 1996
- on 961112,water Gas Decay Tank Oxygen Analyzer Pressure Sensors Inoperable Due to Vendor Supplied Equipment Not Meeting Procurement specifications.Post-implementation Procedures Revised & Transducers Replaced
05000280/LER-1996-007, :on 960821,failed to Complete Fire Detection Zone Inspections within Required Time Period.Caused by Personnel Error.Counseled Personnel Re Fire Detection Zone Inspections & Revised Fire Watch Training1996-09-19019 September 1996
- on 960821,failed to Complete Fire Detection Zone Inspections within Required Time Period.Caused by Personnel Error.Counseled Personnel Re Fire Detection Zone Inspections & Revised Fire Watch Training
05000281/LER-1996-005-01, :on 960803,manual Reactor Trip.Caused by Loss of Electro Hydraulic Control Pressure.Repaired Two Compression Fitting Union Connections on Leaking Fitting & Performed Evaluations on Other Tubing1996-08-26026 August 1996
- on 960803,manual Reactor Trip.Caused by Loss of Electro Hydraulic Control Pressure.Repaired Two Compression Fitting Union Connections on Leaking Fitting & Performed Evaluations on Other Tubing
05000280/LER-1996-006, :on 960618,anti-corrosion Coating Had Not Been Reapplied to Station Battery 2B.Caused by Procedural Error in That Verbatim TS Compliance Not Reflected in Procedures. Coating Was Applied to Batteries1996-07-30030 July 1996
- on 960618,anti-corrosion Coating Had Not Been Reapplied to Station Battery 2B.Caused by Procedural Error in That Verbatim TS Compliance Not Reflected in Procedures. Coating Was Applied to Batteries
05000281/LER-1996-004-02, :on 960606,turbine/reactor Trip Occurred.Caused by High Level in Steam Generator B.Placed Plant in Hot Shutdown Condition,Calculated Shutdown Margin & Monitored Critical Safety Function Status Trees1996-07-0202 July 1996
- on 960606,turbine/reactor Trip Occurred.Caused by High Level in Steam Generator B.Placed Plant in Hot Shutdown Condition,Calculated Shutdown Margin & Monitored Critical Safety Function Status Trees
05000280/LER-1996-004, :on 960510,noticed That Hydrogen Analyzers Inoperable.Caused by Procedural Deficiencies Due to Personnel Error.Permanent Changes to Hydrogen Analyzer Instrument Calibr Procedures Implemented1996-06-10010 June 1996
- on 960510,noticed That Hydrogen Analyzers Inoperable.Caused by Procedural Deficiencies Due to Personnel Error.Permanent Changes to Hydrogen Analyzer Instrument Calibr Procedures Implemented
05000281/LER-1996-003-01, :on 960512,Unit 2 Pressurizer Safety Valve as Found Lift Setting Out of Tolerance.Valve Was Reassembled & Lift Setting Was Established & Tested Satisfactorily1996-06-0707 June 1996
- on 960512,Unit 2 Pressurizer Safety Valve as Found Lift Setting Out of Tolerance.Valve Was Reassembled & Lift Setting Was Established & Tested Satisfactorily
1999-08-27
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18152A2811999-10-12012 October 1999 Technical Basis for Elimination of Nozzle Inner Radius Insps (for Nozzles Other than Reactor Vessel),Technical Basis for ASME Section XI Code Case N-619 05000281/LER-1999-004-02, :on 981109,EDG Was Inoperable Longer than Allowed by TS Due to Governor Compensation Valve.Root Cause Evaluation Being Performed to Determine How Compensation Valve Became Closed1999-10-0101 October 1999
- on 981109,EDG Was Inoperable Longer than Allowed by TS Due to Governor Compensation Valve.Root Cause Evaluation Being Performed to Determine How Compensation Valve Became Closed
ML18152B3531999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Surry Power Station,Units 1 & 2.With ML18152B3371999-09-24024 September 1999 SER Accepting Third 10-year Interval Inservice Insp Plan Request for Relief SR-026 for Surry Power Station Unit 2 ML18152B6651999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Surry Power Station Units 1 & 2.With 05000280/LER-1999-006, :on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With1999-08-27027 August 1999
- on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With
05000280/LER-1999-005-01, :on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed1999-08-27027 August 1999
- on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed
ML18152B3841999-08-23023 August 1999 Safety Evaluation Granting Relief Request from ASME Section Xa Requirements for Containment Insp ML18152B3631999-08-23023 August 1999 Safety Evaluation Supporting Eddy Current Techniques Used by VEPCO to Determine Depth of Degradation Evident in Units SG Tubing & VEPCO Approach for Dispositioning Tubes with Avb Wear Indications ML18152B3831999-08-23023 August 1999 Safety Evaluation Granting Relief Request from ASME Section XI Requirements for Containment Insp 05000280/LER-1999-004-01, :on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms1999-08-13013 August 1999
- on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms
ML18151A3981999-08-13013 August 1999 SPS Unit 2 ISI Summary Rept for 1999 Refueling Outage ML18152B3791999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Surry Power Station,Units 1 & 2.With 05000281/LER-1999-003-02, :on 990705,auto Reactor Trip on Low Coolant Flow,Occurred.Caused by Loop Stop Valve Failure.Approved RCE Recommendations,Designed to Prevent Recurrence of Similar Event Will Be Implemented Through CAP1999-07-30030 July 1999
- on 990705,auto Reactor Trip on Low Coolant Flow,Occurred.Caused by Loop Stop Valve Failure.Approved RCE Recommendations,Designed to Prevent Recurrence of Similar Event Will Be Implemented Through CAP
ML20196J4781999-07-0101 July 1999 Safety Evaluation Supporting Amends 221 & 221 to Licenses DPR-32 & DPR-37,respectively ML18152B3911999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Surry Power Station,Units 1 & 2.With ML20195D3571999-06-0707 June 1999 Safety Evaluation Supporting Amends 220 & 220 to Licenses DPR-32 & DPR-37,respectively ML20195E2401999-05-31031 May 1999 Rev 2 to COLR for SPS Unit 2 Cycle 16 Pattern Ag ML18152B4341999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Surry Power Station,Units 1 & 2.With 05000281/LER-1999-002-02, :on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With1999-05-18018 May 1999
- on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With
ML18152B4161999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Surry Power Station Units 1 & 2.With 05000280/LER-1999-003-01, :on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With1999-04-28028 April 1999
- on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With
ML18152B6481999-04-14014 April 1999 Safety Evaluation Supporting Relief Requests IWE-2,4.5.6 & IWL-2 to Licenses DPR-32 & DPR-37 Respectively ML18152B6451999-04-13013 April 1999 SER Accepting Util Reactor Pressure Vessel Fluence Methodology for Surry Power Stations,Units 1 & 2 & North Anna Power Station,Units 1 & 2 Subject to Listed Limitations 05000281/LER-1999-001-02, :on 990301,RPS Relay Not Placed in Trip Resulted in Violation of TS 3.7.Caused by Lack of Procedural Guidance.Developed New Procedure to Provide More Explicit Instructions for Placing Stop Valve in Relay Trip1999-03-31031 March 1999
- on 990301,RPS Relay Not Placed in Trip Resulted in Violation of TS 3.7.Caused by Lack of Procedural Guidance.Developed New Procedure to Provide More Explicit Instructions for Placing Stop Valve in Relay Trip
ML18152B6511999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Surry Power Station Units 1 & 2 05000280/LER-1999-002-01, :on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 9902121999-03-29029 March 1999
- on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212
05000280/LER-1998-013, :on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr1999-03-19019 March 1999
- on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr
ML20207L8081999-03-12012 March 1999 Safety Evaluation Supporting Amends 219 & 219 to Licenses DPR-32 & DPR-37 ML18152B7331999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Surry Power Station,Units 1 & 2.With ML18152B5381999-02-16016 February 1999 SER Accepting Third 10-year Interval Inservice Insp Request for Relief for Surry Power Station,Unit 1.Staff Concludes That Licensee Proposed Alternative Will Provide Acceptable Level of Quality & Safety.Technical Ltr Rept Also Encl ML18152B5421999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Surry Power Station,Units 1 & 2.With ML18151A3031999-01-29029 January 1999 ISI Summary Rept for 1998 Refueling Outage,Including Form NIS-1, Owners Rept for ISIs & Form NIS-2, Owners Rept for Repairs & Replacements 05000280/LER-1999-001, :on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable1999-01-21021 January 1999
- on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable
ML18152B6011998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Surry Power Station,Units 1 & 2.With ML18152B5861998-12-18018 December 1998 SER Approving Request Relief Related to Inservice Testing Program at Surry Power Station Unit 1 ML20198F9221998-12-16016 December 1998 Safety Evaluation Supporting Amends 217 & 217 to Licenses DPR-32 & DPR-37,respectively 05000280/LER-1998-014, :on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition1998-12-16016 December 1998
- on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition
ML18152B5901998-12-16016 December 1998 Safety Evaluation Authorizing Request to Use Code Case N-577 as Alternative to Requirements of ASME Code Section XI for Surry Power Station,Unit 1 ML18152B7121998-12-0404 December 1998 LER 98-S01-00:on 981105,noted Failure to Deactivate Station Access Badge.Caused by Human Error.Licensee Will Now Deactivate Station Badges Before Clearance Is Revoked & Process for Badge Deactivations Have Been Strengthened 05000280/LER-1998-012, :on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With1998-12-0101 December 1998
- on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With
ML18152B7081998-11-30030 November 1998 Rev 0 to COLR for Surry 1 Cycle 16,Pattern Un ML18152B5721998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Surry Power Station,Units 1 & 2.With ML18152B6241998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Surry Power Station Units 1 & 2.With ML18152B6881998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Surry Power Station Units 1 & 2.With ML20151U7261998-09-0303 September 1998 Safety Evaluation Approving Exemption from Certain 10CFR20 Requirements Re Use of self-contained Breathing Apparatus with Enriched Oxygen in Subatmospheric Containments at SPS ML18153A3271998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Surry Power Station,Units 1 & 2 ML20237E9721998-08-26026 August 1998 Safety Evaluation Supporting Amends 216 & 216 to Licenses DPR-32 & DPR-37,respectively ML18153A3161998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Surry Power Station Units 1 & 2 05000280/LER-1998-010, :on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status1998-07-31031 July 1998
- on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status
1999-09-30
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October 5, 1990 U. S. Nuclear Regulatory Commission Document Control Desk Washington, D. C. 20555 Gentlemen:
Virginia Electric and* Power Company Surry Power Station P. 0. Box 315 Surry, Virginia 23883 Serial No.:
Docket Nos.:
License Nos.:
90-619 50-280 50-281 DPR-32 DPR-37 Pursuant to Surry Power Station Technical Specifications, Virginia Electric and Power Company hereby submits the following Licensee Event Report for Units 1
REPORT NUMBER 90-012-00 This report has been reviewed by the Station Nuclear Safety and Operating Committee and will be reviewed by Corporate Nuclear Safety.
Enclosure cc:
Regional Administrator Suite 2900 101 Marietta Street, NW Atlanta, Georgia 30323 901.0.0!:;;
0~.5000:2:::0 PDC
',)
NRC FORM366 (6-89)
FACILITY NAME (1)
U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)
APPROVED 0MB NO. 3150-0104 EXPIRES: 4/30/92 E
ATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P-530), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0.104)., OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
Surry Power Station, Units 1_ and 2 I
DOCKET NUMBER (2)
I PAGE (3) 0151010101 2 18 1 0 1 loF 013 TITLE 141 Common Mode Failure Mechanism Due to Marine Growth Identified for ESWPs EVENT DATE (6)
LER NUMBER (6)
REPORT DATE (7)
OTHER FACILITIES INVOLVED (8)
MONTH DAY YEAR YEAR }tt sez~~~~~AL (? ~~~~~~. MONTH DAY YEAR FACILITY NAMES DOCKET NUMBERIS) 01s1010101 I
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I OPERATING MODE (9)
N THIS REPORT IS SUBMITTED PURSUANT TO_THE Rl:QUIREMENTS OF _10 CFR §: /Ch~k an* or mare of the fal/awin11/ (11) 20.402(bl 20,405(c) 60.73(ol(21(iv) 20.405(ol(1)(i) 60.31(clC1l
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LICENSEE CONTACT FOR THIS LER 112)
NAME TELEPHONE NUMBER AREA CODE M. R. Kansler, Station Manager
- 8. I O 14 31 5 17 1-I 3 tl I 81 4
CAUSE
SYSTEM COMPONENT C
BI I I
I I
I COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
MANUFAC-TURER I I I
SUPPLEMENTAL REPORT EXPECTED (14)
COMPONENT '
I I
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I I
I I I MONTH DAY YEAR n YES (If ye,, campl*t* EXPECTED ~UBMISSION DATEi
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I ABSTRACT (Limit ta 1400,,,.ce,, i.e., *ppraxim*toly fiftHn 1ingle-,,,.ce typewritton lin*sl (18)
NRC Form 366 (6-89)
On September 6, 1990 with Unit 1 at 74% power and Unit 2 at 100% power, the Emergency Service Water
- Pump, 1-SW-P-lA, was declared inoperable when its flow rate was too low to meet the acceptanc~
criterion of 1-PT-25.3A.
On September 9, 1990 with both units at the same conditions as above, the Emergency Service Water Pump, 1-SW-P-lC, was declared inoperable when its flow rate was too low to meet the acceptance criterion of 1-PT-25.3C.
In both cases, the cause of the problem was determined to be marine growth on the impellers and pump suctions. Following maintenance activities, both pumps passed their performance tests and are back in service.
In accordance with 10CFR50. 73(a)(2)(vii), any event where a single cause or condition that can cause two independent trains or channels to become inoperable in a single system designed to mitigate the consequences of an accident is a reportable event.
A IMIII 1,
FACILITY NAMl 111 U.1. NUCLlAll l'IEOULATOIIY COMMISSION LICENSEE EVE-REPORT CLER)
TEXT CONTINUATION DOCKET NUMIEII 121 APPROVED OMI NO. :11M>-0104 IXPIIIU: 4IJQlll2 TED IUADEN PEfl IIEm'ONIE TO COMPLY WTH THIS MATION COLLECTION IIEOUEST: IO.O HAS. FORWAflD CDMMENTI IIEGAflDING IUIIDEN ESTIMATE TD THE IIECOIIOS NtlD flEPORTI MANAGEMENT IIIANCH IP~I. u.a. NUCUAII IIIEGULATOIIY COMMISSION, WASHINGTON, DC 2CHI, AND TO THE PAPE,iw()flllt IIEDUCTION PIIO.lfCT l:11IIO.Q1041, OFPICE OF MANAGEMENT AND IUDGET, WASHINGTON, DC 20!50l.
LIii NUMIIR Ill PAOI 1:11 Surry Power Station, Units 1 and 2 o 1s10101a.121s1 o 910 -o 111 2- 010 012 OF ol3
- 1. o DESCRIPTION OF THE EVENT On September 6, 1990 with Unit 1 at 74% power and Unit 2 at 100% power, the Emergency Service Water Pump (ESWP) (EIIS-BI,P), 1-SW-P-lA, was declared inoperable due - to a low flow rate of 12,450 gpm.
The acceptance criterion of 1-PT-25.3A is 16,785-17,989 gpm. The next day,
- divers removed hydroids, a marine growth, from the suction of the II A 11 ESWP.
The results of the test later that day were acceptable.
Because of the problems with the 11A 11 ESWP, it was decided to test the 11B" and 11C 11 pumps ahead of their regularly scheduled times.
On September 8, 1990, the 11B" ESWP passed its surveillance test.
On September 9, 1990 with both units at the same conditions as above, the ESWP, 1-SW-P-lC, was declared inoperable due to a low flow rate of 15,249 gpm.
The acceptance criterion of 1-PT-25.3C is 16,435-17,619 gpm.
The "C" ESWP was partially disassembled and the endbell, impeller, and diffuser were cleaned of hydroids and barnacles.
The pump was reassembled and retested on September 13, 1990 with satisfactory results.
In both cases, the cause of the failed performance tests was accumulated marine growth of hydroids and barnacles on the impeller and the suction of the pumps.
After removal of the marine growth, both pumps achieved acceptable results.
According to 10CFR50.73(a)(2)(vii), any event where a single cause or condition that can cause two independent trains or channels to become inoperable in a single system designed to mitigate the consequences of an accident is a reportable event.
The ESWPs provide the source of water to the intake canal during the design basis accident.
- 2. O
SAFETY CONSEQUENCES AND IMPLICATIONS
NIIC,_ aA C..al The ESWPs provide the source of water *10 the intake canal during the design basis accident.
A review of the design basis calculation for intake canal inventory shows the degraded ESWPs met the minimum flow rate required to meet the design basis criteria.
The review shows that a flow rate of 25,350 gpm from two ESWPs will provide adequate inventory to remain within the parameters of* the design basis assumptions.
The total flow rate provided by the "A 11 and "C" ESWP during the performance tests was 27,699 gpm.
In addition, since
NIICfOIIM..
A fM81 FACILITY NAME _CU U.1. NUCUAII IIEGUUTOIIY COMMISSION LICENSEE EVEh.EPORT (LERI TEXT CONTINUATION DOCKET NUMIEII 121
"""OVEO OMI NO. :uao,0104 IXPIIIU:~
EO IUIIDEN,Ell IIUl'ONSE TO COWL Y WTH THIS ATION COLLECTION IIEOUEST: IO.O HRI. fORWAl'ID mllMENTI IIEGMDING IUIIDEI\\I HTIMATE TO THE l'IECOl'IDS AND IIE,ORTI MANAGEMENT IIIANCH IP-6301. U.I. NUCLl!NI IIEGULATOIIY COMMISSION. WAIHINGTON, DC 2CJIM. AND TO
'INE,A,EIIWOflK l'IEOUCTION NIO.ll!CT 131!50410tl. OFPICE OF MANAGEMENT AND IUDGET. WASHINGTON. DC 2QI03, LIii NUMalll Ill
- SE QUINT I AL ::~::::: lflEV8ION NUMe[II
.:::::::::.. u.. *111
,~011'1 Surry Power Station, Units 1 and 2 o Is I o I o I o I 21 s Io 9 Io - o I 1 I 2 o lo o I 3 oF o 13 ffXT r* _,,,_ * ~
MldlrlotW NltC fonn -..*a11171 IIIIC *- INA Cl,GI the "B" ESWP had passed its performance test on September 8, 1990 and was fully -operable, adequate cooling water would have been provided by any two of the ESWPs if a design.basis accident had occurred even with the degraded conditions of the "A" and "C" pumps.
This condition did not adversely affect the plants design basis.
Therefore, the health
- and safety of the public was not affected.
- 3. O
CAUSE OF THE EVENT
The degraded condition of the "A" and "C" ESWP was the result of accumulated marine growth of hydroids and barnacles.
This marine growth increased the flow resistance and mechanical friction within the pumps reducing the pumps' flow rate.
The pumps degraded. to the point where they could not meet the acceptance. criterfa of the required performance tests.
- 4. O IMMEDIATE CORRECTIVE ACTION<S}
5.0 6.0 7.0 The "B" and "C" ESWPs were surveillance tested ahead of their regularly scheduled times.
The marine growth was removed from the suction of the "A" ESWP by divers.
The "C" ESWP was partially disassembled and internally cleaned* of hydroids and barnacles.
Both pumps passed the subsequent tests.
ADDITIONAL CORRECTIVE ACTION<S}
The "B" ESWP suction was cleaned of hydroids by divers on September 20,- 1990.
ACTIONS TO PREVENT RECURRENCE An engineering evaluation is under* way to
- find a long term solution to this problem.
In the interim, the pump. testing frequency wiH be increased to once a month to more closely monitor pump perfm:mance.
Appropriate actions will be taken based oil the results of the evaluation.
SI?4ILAR EVENTS None.
- 8. O -MANUFACTURER/MODEL NUMBER NIA
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05000281/LER-1990-001-01, :on 900108,one of Three RCS Average Temp Channel Inputs to Reactor Protection Sys Not Declared Inoperable After Deviating from Other Two Channels.Caused by Faulty Summator.Summator Replaced |
- on 900108,one of Three RCS Average Temp Channel Inputs to Reactor Protection Sys Not Declared Inoperable After Deviating from Other Two Channels.Caused by Faulty Summator.Summator Replaced
| | 05000280/LER-1990-001-03, :on 900314,emergency Svc Water Pumps Declared Inoperable Due to Emergency Shutdown Device Being in Tripped Condition.Caused by Procedural & Training Deficiencies. Procedures Changed & Training Enhanced |
- on 900314,emergency Svc Water Pumps Declared Inoperable Due to Emergency Shutdown Device Being in Tripped Condition.Caused by Procedural & Training Deficiencies. Procedures Changed & Training Enhanced
| | 05000281/LER-1990-002-01, :on 900205,two Control Rods of Control Bank D Differed from Rod Group Demand Counter by Greater than 12 Steps.Caused by Inadequate Procedures.Rampdown Stopped & Individual Rod Position Indicators Adjusted |
- on 900205,two Control Rods of Control Bank D Differed from Rod Group Demand Counter by Greater than 12 Steps.Caused by Inadequate Procedures.Rampdown Stopped & Individual Rod Position Indicators Adjusted
| | 05000280/LER-1990-002-02, :on 900315,containment Vacuum Pump Auto Started But Tripped Immediately.Caused by Binding of Pump Internals Due to Moisture Accumulation.New Pump Installed.Pumps Will Be Inspected on Periodic Basis |
- on 900315,containment Vacuum Pump Auto Started But Tripped Immediately.Caused by Binding of Pump Internals Due to Moisture Accumulation.New Pump Installed.Pumps Will Be Inspected on Periodic Basis
| | 05000280/LER-1990-003, :on 900323,low Pressure Heater Drain Sys Pipe Leak Occurred Due to Excessive Pipe Wall Thinning |
- on 900323,low Pressure Heater Drain Sys Pipe Leak Occurred Due to Excessive Pipe Wall Thinning
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000281/LER-1990-003-02, :on 900531,reactor Trip Initiated When Malfunction of Main Feedwater Regulating Valve a Positioner Caused Valve to Close.Caused by Buildup of Dirt on Positioner.Positioner Replaced & Data Reviewed |
- on 900531,reactor Trip Initiated When Malfunction of Main Feedwater Regulating Valve a Positioner Caused Valve to Close.Caused by Buildup of Dirt on Positioner.Positioner Replaced & Data Reviewed
| | 05000280/LER-1990-003-01, :on 900323,heater Drain Sys Pipe Leak Developed Downstream Into Unit 1 Turbine Bldg,Causing Halon Sys for Emergency Switchgear Room to Spuriously Actuate.Caused by Pipe Failure.Halon Sys Recharged |
- on 900323,heater Drain Sys Pipe Leak Developed Downstream Into Unit 1 Turbine Bldg,Causing Halon Sys for Emergency Switchgear Room to Spuriously Actuate.Caused by Pipe Failure.Halon Sys Recharged
| | 05000281/LER-1990-004-01, :on 900827,main Feedwater Regulating Valve Closed Following Inadvertent Grounding of Control Signal. Root Cause Not Determined.Computer Multiplexer Testing Procedures Changed |
- on 900827,main Feedwater Regulating Valve Closed Following Inadvertent Grounding of Control Signal. Root Cause Not Determined.Computer Multiplexer Testing Procedures Changed
| | 05000280/LER-1990-004-03, :on 900522,reactor Trip/Turbine Trip Occurred. Caused by Inadvertent Actuation on a Main Transformer. C/A:Main Transformer Was Inspected |
- on 900522,reactor Trip/Turbine Trip Occurred. Caused by Inadvertent Actuation on a Main Transformer. C/A:Main Transformer Was Inspected
| | 05000281/LER-1990-005-03, :on 901120,rod Control Cluster Assembly M-12 Declared Inoperable Due to Mismatch Between Group & Rod Position Indication.Caused by Control Rod Positioned Two Steps from Bottom of Core |
- on 901120,rod Control Cluster Assembly M-12 Declared Inoperable Due to Mismatch Between Group & Rod Position Indication.Caused by Control Rod Positioned Two Steps from Bottom of Core
| | 05000280/LER-1990-005-01, :on 900621,containment Pressure Channel Rendered Inoperable & Not Placed in Trip Condition.Caused by Inadequate Procedure Change to Troubleshooting Procedures. Procedures Written for Venting Lines |
- on 900621,containment Pressure Channel Rendered Inoperable & Not Placed in Trip Condition.Caused by Inadequate Procedure Change to Troubleshooting Procedures. Procedures Written for Venting Lines
| | 05000280/LER-1990-006-01, :on 900701,station Svc Transformer Tripped Due to Actuation of Sudden Pressure Relay.Caused by Grounded Terminal in Sudden Pressure Relay Connector.Emergency & Abnormal Procedures Implemented |
- on 900701,station Svc Transformer Tripped Due to Actuation of Sudden Pressure Relay.Caused by Grounded Terminal in Sudden Pressure Relay Connector.Emergency & Abnormal Procedures Implemented
| | 05000280/LER-1990-007-01, :on 900628,determined That Fire Protection Surveillance Procedure Verifying Operability of Fire Dampers Not Completed within Required Grace Period,Per Tech Specs. Caused by Administrative Oversight |
- on 900628,determined That Fire Protection Surveillance Procedure Verifying Operability of Fire Dampers Not Completed within Required Grace Period,Per Tech Specs. Caused by Administrative Oversight
| | 05000280/LER-1990-008-01, :on 900727,determined That RCS Leakage Greater than 10 Gpm as Indicated by Level Drop on Vol Control Tank Level Recorder.Caused by Broken Gage Sensing Line in Letdown Sys.Sensing Line Repaired |
- on 900727,determined That RCS Leakage Greater than 10 Gpm as Indicated by Level Drop on Vol Control Tank Level Recorder.Caused by Broken Gage Sensing Line in Letdown Sys.Sensing Line Repaired
| | 05000280/LER-1990-009-01, :on 900810 & 29,containment Vacuum Pump Flow Paths Became Inoperable.Caused by Failure of Process Vent Normal Range Radiation Monitor Due to Defective Flow Switch & Failed Cpu Card.Components Replaced |
- on 900810 & 29,containment Vacuum Pump Flow Paths Became Inoperable.Caused by Failure of Process Vent Normal Range Radiation Monitor Due to Defective Flow Switch & Failed Cpu Card.Components Replaced
| | 05000280/LER-1990-010-01, :on 900913,testing Intervals for Type B & Type C Valves Exceeded Due to 10CFR50,App J Interpretation.W/ |
- on 900913,testing Intervals for Type B & Type C Valves Exceeded Due to 10CFR50,App J Interpretation.W/
| | 05000280/LER-1990-011, :on 901004,main Steam Safety Valves Out of Tolerance Due to Minor Setpoint Drift |
- on 901004,main Steam Safety Valves Out of Tolerance Due to Minor Setpoint Drift
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000280/LER-1990-012, :on 900909,common Mode Failure Mechanism Due to Marine Growth Identified for Emergency Svc Water Pump |
- on 900909,common Mode Failure Mechanism Due to Marine Growth Identified for Emergency Svc Water Pump
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | 05000280/LER-1990-013, :on 900928,licensee Failed to Obtain Wgdt Sample within Tech Spec Sampling Interval |
- on 900928,licensee Failed to Obtain Wgdt Sample within Tech Spec Sampling Interval
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000280/LER-1990-014, :on 901023,Units 1 & 2 Recirculation Spray HXs Declared Inoperable Due to Potentially Inadequate Svc Water Flow,Caused by Macrofouling.Supply Piping to Recirculation Spray HXs Inspected & Cleaned |
- on 901023,Units 1 & 2 Recirculation Spray HXs Declared Inoperable Due to Potentially Inadequate Svc Water Flow,Caused by Macrofouling.Supply Piping to Recirculation Spray HXs Inspected & Cleaned
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000280/LER-1990-015, :on 901018,hydrogen Analyzer Surveillance Testing Was Performed Due to Misinterpretation of Tech Spec Requirements |
- on 901018,hydrogen Analyzer Surveillance Testing Was Performed Due to Misinterpretation of Tech Spec Requirements
| | 05000280/LER-1990-016, :on 901122,during Cold Shutdown for Refueling, Determined That Type C Leakage Testing Exceeded Maximum Allowable Values Specified by 10CFR50 App J.Caused by Cycling of Valves.Valves Repaired |
- on 901122,during Cold Shutdown for Refueling, Determined That Type C Leakage Testing Exceeded Maximum Allowable Values Specified by 10CFR50 App J.Caused by Cycling of Valves.Valves Repaired
| 10 CFR 50.73(o)(2)(v) | 05000280/LER-1990-017, :on 901202,loss of 4,160-volt Transfer Bus F Occurred.Caused by Personnel Error.Appropriate Training & Procedural Enhancements Are Being Undertaken |
- on 901202,loss of 4,160-volt Transfer Bus F Occurred.Caused by Personnel Error.Appropriate Training & Procedural Enhancements Are Being Undertaken
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000280/LER-1990-018, :on 901203,unplanned Initiation of ESF & SI Occurred During Performance of Operations Periodic Test. Caused by Inadequate Test Procedure.Personnel Preparing & Reviewing Test Procedures Will Be Cautioned |
- on 901203,unplanned Initiation of ESF & SI Occurred During Performance of Operations Periodic Test. Caused by Inadequate Test Procedure.Personnel Preparing & Reviewing Test Procedures Will Be Cautioned
| | 05000280/LER-1990-019, :on 901218,all Six Main Feedwater Flow Transmitters Found Isolated,Equalized & Drained.Caused by Personnel Error.Policy Re Personnel Responsible for Performing Valve Manipulation Will Be Reviewed |
- on 901218,all Six Main Feedwater Flow Transmitters Found Isolated,Equalized & Drained.Caused by Personnel Error.Policy Re Personnel Responsible for Performing Valve Manipulation Will Be Reviewed
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | 05000280/LER-1990-020, :on 910306,containment Spray Pump Discharge Pressure Switch Declared Inoperable Based on Results of Mgt Review.Caused by Weakness in Preventive Maint Program. Pressure Switches Involved Tested |
- on 910306,containment Spray Pump Discharge Pressure Switch Declared Inoperable Based on Results of Mgt Review.Caused by Weakness in Preventive Maint Program. Pressure Switches Involved Tested
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(o)(2) |
|