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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000281/LER-1999-004-02, :on 981109,EDG Was Inoperable Longer than Allowed by TS Due to Governor Compensation Valve.Root Cause Evaluation Being Performed to Determine How Compensation Valve Became Closed1999-10-0101 October 1999
- on 981109,EDG Was Inoperable Longer than Allowed by TS Due to Governor Compensation Valve.Root Cause Evaluation Being Performed to Determine How Compensation Valve Became Closed
05000280/LER-1999-006, :on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With1999-08-27027 August 1999
- on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With
05000280/LER-1999-005-01, :on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed1999-08-27027 August 1999
- on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed
05000280/LER-1999-004-01, :on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms1999-08-13013 August 1999
- on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms
05000281/LER-1999-003-02, :on 990705,auto Reactor Trip on Low Coolant Flow,Occurred.Caused by Loop Stop Valve Failure.Approved RCE Recommendations,Designed to Prevent Recurrence of Similar Event Will Be Implemented Through CAP1999-07-30030 July 1999
- on 990705,auto Reactor Trip on Low Coolant Flow,Occurred.Caused by Loop Stop Valve Failure.Approved RCE Recommendations,Designed to Prevent Recurrence of Similar Event Will Be Implemented Through CAP
05000281/LER-1999-002-02, :on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With1999-05-18018 May 1999
- on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With
05000280/LER-1999-003-01, :on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With1999-04-28028 April 1999
- on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With
05000281/LER-1999-001-02, :on 990301,RPS Relay Not Placed in Trip Resulted in Violation of TS 3.7.Caused by Lack of Procedural Guidance.Developed New Procedure to Provide More Explicit Instructions for Placing Stop Valve in Relay Trip1999-03-31031 March 1999
- on 990301,RPS Relay Not Placed in Trip Resulted in Violation of TS 3.7.Caused by Lack of Procedural Guidance.Developed New Procedure to Provide More Explicit Instructions for Placing Stop Valve in Relay Trip
05000280/LER-1999-002-01, :on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 9902121999-03-29029 March 1999
- on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212
05000280/LER-1998-013, :on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr1999-03-19019 March 1999
- on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr
05000280/LER-1999-001, :on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable1999-01-21021 January 1999
- on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable
05000280/LER-1998-014, :on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition1998-12-16016 December 1998
- on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition
ML18152B7121998-12-0404 December 1998 LER 98-S01-00:on 981105,noted Failure to Deactivate Station Access Badge.Caused by Human Error.Licensee Will Now Deactivate Station Badges Before Clearance Is Revoked & Process for Badge Deactivations Have Been Strengthened 05000280/LER-1998-012, :on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With1998-12-0101 December 1998
- on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With
05000280/LER-1998-010, :on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status1998-07-31031 July 1998
- on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status
05000280/LER-1998-009, :on 980509,nonisolable Leak of Reactor Coolant Pump Seal Injection Line Weld,Was Discovered.Caused by Lack of Fusion or Thermal Fatigue Coupled W/Vibration Stress Due to Loose Rod Hanger.Rcp Seal Injection Line Removed1998-06-0303 June 1998
- on 980509,nonisolable Leak of Reactor Coolant Pump Seal Injection Line Weld,Was Discovered.Caused by Lack of Fusion or Thermal Fatigue Coupled W/Vibration Stress Due to Loose Rod Hanger.Rcp Seal Injection Line Removed
05000280/LER-1998-008, :on 980228,auxiliary Ventilation Fans Were Noted in Condition Outside of Design Basis.Caused by Failure to Recognize Potential Impact of Certain Design Basis Accident Scenarios.No Corrective Actions Needed1998-05-22022 May 1998
- on 980228,auxiliary Ventilation Fans Were Noted in Condition Outside of Design Basis.Caused by Failure to Recognize Potential Impact of Certain Design Basis Accident Scenarios.No Corrective Actions Needed
05000280/LER-1998-007, :on 980330,radiation Monitors Were Declared Inoperable.Caused by Change in Operating Temperature Range. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-61998-04-29029 April 1998
- on 980330,radiation Monitors Were Declared Inoperable.Caused by Change in Operating Temperature Range. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-6
05000280/LER-1998-006, :on 980324,unisolable Through Wall Leak of RCP Thermowell Was Noted.Cause of Leak Is Unknown.Rtd Will Be Replaced1998-04-22022 April 1998
- on 980324,unisolable Through Wall Leak of RCP Thermowell Was Noted.Cause of Leak Is Unknown.Rtd Will Be Replaced
05000280/LER-1998-005, :on 980212,fire Watch Insp Exceeded One Hour. Caused by Lack of Attention to Detail by Individual Involved.Individual Involved Was Coached on Requirement to Perform Fire Watch Patrols within Required Time Frame1998-04-22022 April 1998
- on 980212,fire Watch Insp Exceeded One Hour. Caused by Lack of Attention to Detail by Individual Involved.Individual Involved Was Coached on Requirement to Perform Fire Watch Patrols within Required Time Frame
05000280/LER-1998-003, :on 980226,no Procedural Guidance for Maintaining EDG Minimum Fuel Supply During Loop,Was Identified.Caused by Absence of Procedural Instructions. Deviation Rept Submitted to Document Deviating Condition1998-03-0909 March 1998
- on 980226,no Procedural Guidance for Maintaining EDG Minimum Fuel Supply During Loop,Was Identified.Caused by Absence of Procedural Instructions. Deviation Rept Submitted to Document Deviating Condition
05000280/LER-1998-004, :on 980206,fire Watch Was Released Prematurely Resulting in Violation of Ts.Caused by Inadequate Planning of Repair Activity.Work Orders Will Include Ref to Applicable Procedures Developed to Assist in Repairs1998-03-0606 March 1998
- on 980206,fire Watch Was Released Prematurely Resulting in Violation of Ts.Caused by Inadequate Planning of Repair Activity.Work Orders Will Include Ref to Applicable Procedures Developed to Assist in Repairs
05000280/LER-1998-002, :on 980202,automatic Turbine Trip Resulted in Automatic Reactor Trip.Caused Degraded Generator Voltage Regulator sub-component Failure.Placed Plant in Safe Hot SD & Replaced Intermittent Relay & Relay Socket1998-03-0404 March 1998
- on 980202,automatic Turbine Trip Resulted in Automatic Reactor Trip.Caused Degraded Generator Voltage Regulator sub-component Failure.Placed Plant in Safe Hot SD & Replaced Intermittent Relay & Relay Socket
05000280/LER-1998-001-01, :on 980108,deficient Test Due to Faulty Test Equipment Resulted in TS Violation.Caused by Faulty Vibration Analyzer Cable or Loose Connection.Station Deviation Rept Was Submitted1998-02-0606 February 1998
- on 980108,deficient Test Due to Faulty Test Equipment Resulted in TS Violation.Caused by Faulty Vibration Analyzer Cable or Loose Connection.Station Deviation Rept Was Submitted
05000280/LER-1997-009, :on 971014,declared Intake Canal Level Probes Inoperable Due to Marine Growth.Caused by Inadequate Maint of Intake Canal Level Probes.Subject Probes Were Cleaned, Tested Satisfactorily & Returned to Operable Status1998-01-13013 January 1998
- on 971014,declared Intake Canal Level Probes Inoperable Due to Marine Growth.Caused by Inadequate Maint of Intake Canal Level Probes.Subject Probes Were Cleaned, Tested Satisfactorily & Returned to Operable Status
05000280/LER-1997-012, :on 971028,loss of Power to Latching Mechanism on Several Doors Occurred.Caused by Tripping of Two Breakers in Security Distribution Panel.Reset Affected Breakers Which Restored Power to Security Systems & Affected Doors1998-01-13013 January 1998
- on 971028,loss of Power to Latching Mechanism on Several Doors Occurred.Caused by Tripping of Two Breakers in Security Distribution Panel.Reset Affected Breakers Which Restored Power to Security Systems & Affected Doors
05000281/LER-1997-004-02, :on 971202,invalid Mstv Indication Results in Manual Reactor Trip W/Esf Actuation Were Noted.Caused by Displaced Open Limit Switch Arms.Open Limit Switch for Mstv a Was Relocated Closer to Valve Position Bar1997-12-31031 December 1997
- on 971202,invalid Mstv Indication Results in Manual Reactor Trip W/Esf Actuation Were Noted.Caused by Displaced Open Limit Switch Arms.Open Limit Switch for Mstv a Was Relocated Closer to Valve Position Bar
05000281/LER-1997-002-01, :on 970713,main Steam High Range Radiation Monitor Was Declared Inoperable.Caused by Equipment Failure. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-61997-12-10010 December 1997
- on 970713,main Steam High Range Radiation Monitor Was Declared Inoperable.Caused by Equipment Failure. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-6
05000280/LER-1997-011, :on 971030,determined That Periodic Test Procedures for Testing Reactor Trip Bypass Breakers Did Not Test Manual Undervoltage Trip.Caused by mis-interpretation of Term in-service. Procedures Revised1997-11-26026 November 1997
- on 971030,determined That Periodic Test Procedures for Testing Reactor Trip Bypass Breakers Did Not Test Manual Undervoltage Trip.Caused by mis-interpretation of Term in-service. Procedures Revised
05000280/LER-1997-010, :on 971028,discovered Missed Fire Protection Surveillance Pt.Caused by Personnel Error.Satisfactorily Completed PT Procedure 0-OPT-FP-009 & Diesel Driven Fire Pump 1-FP-P-2 Declared Operable1997-11-25025 November 1997
- on 971028,discovered Missed Fire Protection Surveillance Pt.Caused by Personnel Error.Satisfactorily Completed PT Procedure 0-OPT-FP-009 & Diesel Driven Fire Pump 1-FP-P-2 Declared Operable
05000281/LER-1997-003-02, :on 971014,Unit 2 MSSVs Revealed That Lift Setting for Two MSSVs Were Outside as Found Setpoint Tolerance.Caused by Minor Setpoint Drift.Repaired,Revised & Adjusted Safety Valves1997-11-13013 November 1997
- on 971014,Unit 2 MSSVs Revealed That Lift Setting for Two MSSVs Were Outside as Found Setpoint Tolerance.Caused by Minor Setpoint Drift.Repaired,Revised & Adjusted Safety Valves
05000280/LER-1997-008-01, :on 971011,invalid Actuation of ESF Occurred. Caused by Personnel Errors.Main CR Bottled Air Sys Isolated & Containment Hydrogen Analyzer Heat Tracing Actuation Signal Reset1997-11-0707 November 1997
- on 971011,invalid Actuation of ESF Occurred. Caused by Personnel Errors.Main CR Bottled Air Sys Isolated & Containment Hydrogen Analyzer Heat Tracing Actuation Signal Reset
05000280/LER-1997-007-01, :on 970930,determined That Plant Was Outside App R Design Basis Due to Vital Bus Isolation Issue.Caused by Personnel Error.Installed Circuit Protective Device During Oct 1997 Refueling Outage1997-10-30030 October 1997
- on 970930,determined That Plant Was Outside App R Design Basis Due to Vital Bus Isolation Issue.Caused by Personnel Error.Installed Circuit Protective Device During Oct 1997 Refueling Outage
05000281/LER-1997-002-03, :on 970713,CR annunciator,2-RMA-A-7 for Main Steam Line Effluent High Range Radiation Monitors Alarmed. Caused by Intermittent Component Failure.Preplanned Alternate Method of Monitoring Initiated1997-08-12012 August 1997
- on 970713,CR annunciator,2-RMA-A-7 for Main Steam Line Effluent High Range Radiation Monitors Alarmed. Caused by Intermittent Component Failure.Preplanned Alternate Method of Monitoring Initiated
05000280/LER-1997-001, :on 970123,shutdown Occurred Due to Drain Line Weld Leak.Inspected & Tested Turbine Trip Actuation Circuitry1997-06-10010 June 1997
- on 970123,shutdown Occurred Due to Drain Line Weld Leak.Inspected & Tested Turbine Trip Actuation Circuitry
05000280/LER-1997-005, :on 970502,Unit 1 Power Range Nuclear Instrumentation Was Inoperable Due to Personnel Error.Sro & STA That Were Involved in Event Were Counseled1997-05-28028 May 1997
- on 970502,Unit 1 Power Range Nuclear Instrumentation Was Inoperable Due to Personnel Error.Sro & STA That Were Involved in Event Were Counseled
05000280/LER-1997-006, :on 970320,loss of Refueling Integrity Due to Inadequate Containment Closure Process & Verification.Fuel Movement Stopped IAW Action Statement Requirements of TS 3.10.B1997-04-18018 April 1997
- on 970320,loss of Refueling Integrity Due to Inadequate Containment Closure Process & Verification.Fuel Movement Stopped IAW Action Statement Requirements of TS 3.10.B
05000280/LER-1997-004, :on 970317,main Steam Safety Valve Was Outside as Found Setpoint Tolerance.Specific Cause Unknown,However, Minor Setpoint Drift Can Be Expected.No Immediate Corrective Actions Performed1997-04-15015 April 1997
- on 970317,main Steam Safety Valve Was Outside as Found Setpoint Tolerance.Specific Cause Unknown,However, Minor Setpoint Drift Can Be Expected.No Immediate Corrective Actions Performed
05000280/LER-1997-002, :on 970116,one Train of Auxiliary Ventilation Sys Was Inoperable Outside of Ts.Caused by Personnel Error. Submitted Deviation Rept Re Reverse Rotation of Fan & Work Request to Adjust Linkage1997-04-0808 April 1997
- on 970116,one Train of Auxiliary Ventilation Sys Was Inoperable Outside of Ts.Caused by Personnel Error. Submitted Deviation Rept Re Reverse Rotation of Fan & Work Request to Adjust Linkage
05000281/LER-1997-001-01, :on 970218,manual Reactor Trip & ESF Actuation Occurred Due to Loss of EHC Control Power.Caused by Momentary Short.Relay Card Was Replaced1997-03-19019 March 1997
- on 970218,manual Reactor Trip & ESF Actuation Occurred Due to Loss of EHC Control Power.Caused by Momentary Short.Relay Card Was Replaced
05000280/LER-1997-003, :on 970219,loss of Pressurizer Heaters Resulted in Manual U1 Trip & U2 ESF Actuation.Caused by Loss of Group C Pressurizer Proportional Heaters.Reactor Trip Breakers Were Verified Open1997-03-19019 March 1997
- on 970219,loss of Pressurizer Heaters Resulted in Manual U1 Trip & U2 ESF Actuation.Caused by Loss of Group C Pressurizer Proportional Heaters.Reactor Trip Breakers Were Verified Open
05000280/LER-1997-002-01, :on 970116,one Train of Auxiliary Ventilation Sys Declared Inoperable.Caused by Personnel Error.Properly Adjusted Damper 1-VS-MOD-58B & Exited Seven Day LCO on 9701161997-02-13013 February 1997
- on 970116,one Train of Auxiliary Ventilation Sys Declared Inoperable.Caused by Personnel Error.Properly Adjusted Damper 1-VS-MOD-58B & Exited Seven Day LCO on 970116
05000281/LER-1997-002, :on 961213,automatic Reactor Trip Occurred During Planned Shutdown.Caused by Steam Flow/Feedwater Flow Mismatch.Rps Functioned as Designed & Plant Placed in Hot Shutdown1997-01-0202 January 1997
- on 961213,automatic Reactor Trip Occurred During Planned Shutdown.Caused by Steam Flow/Feedwater Flow Mismatch.Rps Functioned as Designed & Plant Placed in Hot Shutdown
05000280/LER-1996-008-01, :on 961112,water Gas Decay Tank Oxygen Analyzer Pressure Sensors Inoperable Due to Vendor Supplied Equipment Not Meeting Procurement specifications.Post-implementation Procedures Revised & Transducers Replaced1996-12-12012 December 1996
- on 961112,water Gas Decay Tank Oxygen Analyzer Pressure Sensors Inoperable Due to Vendor Supplied Equipment Not Meeting Procurement specifications.Post-implementation Procedures Revised & Transducers Replaced
05000280/LER-1996-007, :on 960821,failed to Complete Fire Detection Zone Inspections within Required Time Period.Caused by Personnel Error.Counseled Personnel Re Fire Detection Zone Inspections & Revised Fire Watch Training1996-09-19019 September 1996
- on 960821,failed to Complete Fire Detection Zone Inspections within Required Time Period.Caused by Personnel Error.Counseled Personnel Re Fire Detection Zone Inspections & Revised Fire Watch Training
05000281/LER-1996-005-01, :on 960803,manual Reactor Trip.Caused by Loss of Electro Hydraulic Control Pressure.Repaired Two Compression Fitting Union Connections on Leaking Fitting & Performed Evaluations on Other Tubing1996-08-26026 August 1996
- on 960803,manual Reactor Trip.Caused by Loss of Electro Hydraulic Control Pressure.Repaired Two Compression Fitting Union Connections on Leaking Fitting & Performed Evaluations on Other Tubing
05000280/LER-1996-006, :on 960618,anti-corrosion Coating Had Not Been Reapplied to Station Battery 2B.Caused by Procedural Error in That Verbatim TS Compliance Not Reflected in Procedures. Coating Was Applied to Batteries1996-07-30030 July 1996
- on 960618,anti-corrosion Coating Had Not Been Reapplied to Station Battery 2B.Caused by Procedural Error in That Verbatim TS Compliance Not Reflected in Procedures. Coating Was Applied to Batteries
05000281/LER-1996-004-02, :on 960606,turbine/reactor Trip Occurred.Caused by High Level in Steam Generator B.Placed Plant in Hot Shutdown Condition,Calculated Shutdown Margin & Monitored Critical Safety Function Status Trees1996-07-0202 July 1996
- on 960606,turbine/reactor Trip Occurred.Caused by High Level in Steam Generator B.Placed Plant in Hot Shutdown Condition,Calculated Shutdown Margin & Monitored Critical Safety Function Status Trees
05000280/LER-1996-004, :on 960510,noticed That Hydrogen Analyzers Inoperable.Caused by Procedural Deficiencies Due to Personnel Error.Permanent Changes to Hydrogen Analyzer Instrument Calibr Procedures Implemented1996-06-10010 June 1996
- on 960510,noticed That Hydrogen Analyzers Inoperable.Caused by Procedural Deficiencies Due to Personnel Error.Permanent Changes to Hydrogen Analyzer Instrument Calibr Procedures Implemented
05000281/LER-1996-003-01, :on 960512,Unit 2 Pressurizer Safety Valve as Found Lift Setting Out of Tolerance.Valve Was Reassembled & Lift Setting Was Established & Tested Satisfactorily1996-06-0707 June 1996
- on 960512,Unit 2 Pressurizer Safety Valve as Found Lift Setting Out of Tolerance.Valve Was Reassembled & Lift Setting Was Established & Tested Satisfactorily
1999-08-27
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18152A2811999-10-12012 October 1999 Technical Basis for Elimination of Nozzle Inner Radius Insps (for Nozzles Other than Reactor Vessel),Technical Basis for ASME Section XI Code Case N-619 05000281/LER-1999-004-02, :on 981109,EDG Was Inoperable Longer than Allowed by TS Due to Governor Compensation Valve.Root Cause Evaluation Being Performed to Determine How Compensation Valve Became Closed1999-10-0101 October 1999
- on 981109,EDG Was Inoperable Longer than Allowed by TS Due to Governor Compensation Valve.Root Cause Evaluation Being Performed to Determine How Compensation Valve Became Closed
ML18152B3531999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Surry Power Station,Units 1 & 2.With ML18152B3371999-09-24024 September 1999 SER Accepting Third 10-year Interval Inservice Insp Plan Request for Relief SR-026 for Surry Power Station Unit 2 ML18152B6651999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Surry Power Station Units 1 & 2.With 05000280/LER-1999-006, :on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With1999-08-27027 August 1999
- on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With
05000280/LER-1999-005-01, :on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed1999-08-27027 August 1999
- on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed
ML18152B3841999-08-23023 August 1999 Safety Evaluation Granting Relief Request from ASME Section Xa Requirements for Containment Insp ML18152B3631999-08-23023 August 1999 Safety Evaluation Supporting Eddy Current Techniques Used by VEPCO to Determine Depth of Degradation Evident in Units SG Tubing & VEPCO Approach for Dispositioning Tubes with Avb Wear Indications ML18152B3831999-08-23023 August 1999 Safety Evaluation Granting Relief Request from ASME Section XI Requirements for Containment Insp 05000280/LER-1999-004-01, :on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms1999-08-13013 August 1999
- on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms
ML18151A3981999-08-13013 August 1999 SPS Unit 2 ISI Summary Rept for 1999 Refueling Outage ML18152B3791999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Surry Power Station,Units 1 & 2.With 05000281/LER-1999-003-02, :on 990705,auto Reactor Trip on Low Coolant Flow,Occurred.Caused by Loop Stop Valve Failure.Approved RCE Recommendations,Designed to Prevent Recurrence of Similar Event Will Be Implemented Through CAP1999-07-30030 July 1999
- on 990705,auto Reactor Trip on Low Coolant Flow,Occurred.Caused by Loop Stop Valve Failure.Approved RCE Recommendations,Designed to Prevent Recurrence of Similar Event Will Be Implemented Through CAP
ML20196J4781999-07-0101 July 1999 Safety Evaluation Supporting Amends 221 & 221 to Licenses DPR-32 & DPR-37,respectively ML18152B3911999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Surry Power Station,Units 1 & 2.With ML20195D3571999-06-0707 June 1999 Safety Evaluation Supporting Amends 220 & 220 to Licenses DPR-32 & DPR-37,respectively ML20195E2401999-05-31031 May 1999 Rev 2 to COLR for SPS Unit 2 Cycle 16 Pattern Ag ML18152B4341999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Surry Power Station,Units 1 & 2.With 05000281/LER-1999-002-02, :on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With1999-05-18018 May 1999
- on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With
ML18152B4161999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Surry Power Station Units 1 & 2.With 05000280/LER-1999-003-01, :on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With1999-04-28028 April 1999
- on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With
ML18152B6481999-04-14014 April 1999 Safety Evaluation Supporting Relief Requests IWE-2,4.5.6 & IWL-2 to Licenses DPR-32 & DPR-37 Respectively ML18152B6451999-04-13013 April 1999 SER Accepting Util Reactor Pressure Vessel Fluence Methodology for Surry Power Stations,Units 1 & 2 & North Anna Power Station,Units 1 & 2 Subject to Listed Limitations 05000281/LER-1999-001-02, :on 990301,RPS Relay Not Placed in Trip Resulted in Violation of TS 3.7.Caused by Lack of Procedural Guidance.Developed New Procedure to Provide More Explicit Instructions for Placing Stop Valve in Relay Trip1999-03-31031 March 1999
- on 990301,RPS Relay Not Placed in Trip Resulted in Violation of TS 3.7.Caused by Lack of Procedural Guidance.Developed New Procedure to Provide More Explicit Instructions for Placing Stop Valve in Relay Trip
ML18152B6511999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Surry Power Station Units 1 & 2 05000280/LER-1999-002-01, :on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 9902121999-03-29029 March 1999
- on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212
05000280/LER-1998-013, :on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr1999-03-19019 March 1999
- on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr
ML20207L8081999-03-12012 March 1999 Safety Evaluation Supporting Amends 219 & 219 to Licenses DPR-32 & DPR-37 ML18152B7331999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Surry Power Station,Units 1 & 2.With ML18152B5381999-02-16016 February 1999 SER Accepting Third 10-year Interval Inservice Insp Request for Relief for Surry Power Station,Unit 1.Staff Concludes That Licensee Proposed Alternative Will Provide Acceptable Level of Quality & Safety.Technical Ltr Rept Also Encl ML18152B5421999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Surry Power Station,Units 1 & 2.With ML18151A3031999-01-29029 January 1999 ISI Summary Rept for 1998 Refueling Outage,Including Form NIS-1, Owners Rept for ISIs & Form NIS-2, Owners Rept for Repairs & Replacements 05000280/LER-1999-001, :on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable1999-01-21021 January 1999
- on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable
ML18152B6011998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Surry Power Station,Units 1 & 2.With ML18152B5861998-12-18018 December 1998 SER Approving Request Relief Related to Inservice Testing Program at Surry Power Station Unit 1 ML20198F9221998-12-16016 December 1998 Safety Evaluation Supporting Amends 217 & 217 to Licenses DPR-32 & DPR-37,respectively 05000280/LER-1998-014, :on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition1998-12-16016 December 1998
- on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition
ML18152B5901998-12-16016 December 1998 Safety Evaluation Authorizing Request to Use Code Case N-577 as Alternative to Requirements of ASME Code Section XI for Surry Power Station,Unit 1 ML18152B7121998-12-0404 December 1998 LER 98-S01-00:on 981105,noted Failure to Deactivate Station Access Badge.Caused by Human Error.Licensee Will Now Deactivate Station Badges Before Clearance Is Revoked & Process for Badge Deactivations Have Been Strengthened 05000280/LER-1998-012, :on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With1998-12-0101 December 1998
- on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With
ML18152B7081998-11-30030 November 1998 Rev 0 to COLR for Surry 1 Cycle 16,Pattern Un ML18152B5721998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Surry Power Station,Units 1 & 2.With ML18152B6241998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Surry Power Station Units 1 & 2.With ML18152B6881998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Surry Power Station Units 1 & 2.With ML20151U7261998-09-0303 September 1998 Safety Evaluation Approving Exemption from Certain 10CFR20 Requirements Re Use of self-contained Breathing Apparatus with Enriched Oxygen in Subatmospheric Containments at SPS ML18153A3271998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Surry Power Station,Units 1 & 2 ML20237E9721998-08-26026 August 1998 Safety Evaluation Supporting Amends 216 & 216 to Licenses DPR-32 & DPR-37,respectively ML18153A3161998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Surry Power Station Units 1 & 2 05000280/LER-1998-010, :on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status1998-07-31031 July 1998
- on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status
1999-09-30
[Table view] |
text
~,6,11,.a..i.:.t '-:l V ~*'\\..L.
REGULA~ INFORMATION DISTRIBUTIO.YSTEM (RIDS)
=.,-~: ACCESSION NBR:9607110221 DOC.DATE: 96/07/02 NOTARIZED: NO DOCKET#
05000281 FACIL:50-281 Surry Power Station, Unit 2, Virginia Electric & Powe AUTH.NAME AUTHOR AFFILIATION CHRISTIAN,D.A.
Virginia Power (Virginia Electric & Power Co.)
RECIP.NAME RECIPIENT AFFILIATION SUBJECT: LER 96-004-00:on 960606,turbine/reactor trip occurred.Caused by high level in Steam Generator B.Placed plant in hot shutdown condition,calculated shutdown margin & monitored critical safety function status trees.W/960702 ltr.
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR I ENCL J
SIZE: lo TITLE: 50.73/50.9 Licensee Event Report (LER),-Ynciden~Rpt, et-c-.~~~~
NOTES:
RECIPIENT COPIES RECIPIENT ID CODE/NAME LTTR ENCL ID CODE/NAME PD2-l PD 1
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INTERNAL: ACRS 1
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1 NRR/DRCH/HOLB NRR/DRCH/HQMB 1
1 NRR/DRPM/PECB NRR/DSSA/SPLB 1
1 NRR/DSSA/SRXB RES/DSIR/EIB 1
1 RGN2 FILE 01 EXTERNAL: L ST LOBBY WARD 1
1 LITCO BRYCE,J H NOAC MURPHY,G.A 1
1 NOAC POORE,W.
NRC PDR 1
1 NUDOCS FULL TXT NOTES:
1
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L July 2, 1996 U.S. Nuclear Regulatory Commission Document Control Desk Washington, D. C. 20555
Dear Sirs:
10CFR50.73 Virginia Electric and Power Company Surry Power Station 5570 Hog Island Road Surry, Virginia 23883 Serial No.:
96-347 SPS:JDKNLA Docket No.: 50-281 License No.: DPR-37 Pursuant to Surry Power Station Technical Specifications, Virginia Electric and Power Company hereby submits the following Licensee Event Report applicable to Surry Power Station Unit 2.
REPORT NUMBER 50-281 /96-004-00 This report has been reviewed by the Station Nuclear Safety and Operating Committee and will be forwarded to the Management Safety Review Committee for its review.
Very truly yours, D. A. Christian Station Manager Enclosure pc:
Regional Administrator 101 Marietta Street, NW, Suite 2900 Atlanta, Georgia 30323 M. W. Branch NRC Senior Resident Inspector Surry Power Station
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9607110221 960702 PDR ADOCK 05000281 s
PDR
NRG FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY 0MB NO. 3150-0104 (5-92)
EXPIRES 5/31/95 I
ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD LICENSING EVENT REPORT (LER)
COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH (MNBB 7714), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555-0001, AND TO (See reverse for required number of digits/characters for each block)
THE PAPERWORK REDUCTION PROJECT (3150*0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON. DC 20503.
FACILITY NAME (1)
DOCKET NUMBER (2)
II PAGE (3)
SURRY POWER STATION, Unit 2 05000 - 281 1 OF 5 TITLE (4)
Turbine/Reactor Trip due to High Level in the Steam Generator EVENT DATE 5)
LER NUMBER (6 REPORT DATE 7 OTHER FACILITIES INVOLVED 8)
MONTH DAY YEAR YEAR SEQUENTIAL REVISION MONTH DAY YEAR FACILITY NAME DOCKET NUMBER NUMBER NUMBER Surry Unit 1 05000- 280 06 06 96 96
-- 004 --
0 07 02 96 FACILITY NAME DOCKET NUMBER 05000 -
OPERATING THIS REPORT IS SUBMITIED PURSUANT TO THE REQUIREMENTS OF 10 CFR:(Check one or more) (11)
MODE (9) 20.402(b) 20.405(c)
X 50.73(a)(2)(iv) 73.71(c)
POWER 20.405(a)(1 )(i) 50.36(c)(1) 50.73(a)(2)(v) 73.71(c)
LEVEL (10) 16%
20.405(a)(1 )(ii) 50.36(c)(2) 50.73(a)(2)(vii)
OTHER 20.405(a)(1 )(iii) 50.73(a)(2)(i) 50.73(a)(2)(viii)(A)
(Specify in Abstract below and
- \\'.?;Lt";
20.405(a)(1 )(iv)
- 50. 73(a)(2)(ii) 50.73(a)(2)(viii)(B) in Text. NRG Form 366A) 20.405(a)(1 )(v) 50.73(a)(2)(iii) 50.73(a)(2)(x)
LICENSEE CONTACT FOR THIS LEA 12)
NAME I (804r357~3n34ing Area Code)
D. A. Christian, Station Manager COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE
SYSTEM COMPONENT MANUFACTURER REPORTABLE It>>****
CAUSE
SYSTEM COMPONENT MANUFACTURER REPORTABLE TONPRDS TONPRDS h'*
/... '
SUPPLEMENTAL REPORT EXPECTED (14)
I EXPECTED I MONTH I DAY I YEAR I YES (If yes, complete EXPECTED SUBMISSION DATE)
XI NO I
SUBMISSION DATE (15)
I I
I ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16)
On June 6, 1996, power escalation was in progress for Unit 2 upon completion of a scheduled refueling outage. Control Room Operators were transferring from manual feedwater flow control with the Main Feedwater Regulation Valve (MFRV) Bypass Valves to automatic feedwater control with the MFRVs. At 2344 hours0.0271 days <br />0.651 hours <br />0.00388 weeks <br />8.91892e-4 months <br />, with Unit 2 at 16% power, a high-high Steam Generator B level signal automatically tripped the running main feedwater pump and the main turbine.
The turbine trip generated a reactor trip signal.
The Reactor Protection System actuated and functioned as designed, and all control rods inserted into the core. Following the trip, Control Room Operators acted promptly to place the plant in a safe, hot shutdown condition in accordance with the proper procedures.
The Shift Technical Advisor calculated the shutdown margin and monitored the critical safety function status trees to verify that the unit conditions were acceptable.
Plant response was as expected and the unit stabilized at hot shutdown.
During this event the health and safety of the public were not affected. This event is being reported pursuant to 10 CFR 50.73(a)(2)(iv).
NRG FORM 366 (5-92)
.
(5-92)
.S. NUCLEAR REGULATORY COMMISSION LICENSING EVENT REPORT (LER)
(See reverse for required number of digits/characters for each block)
FACILITY NAME C1l DOCKET NUMBER (2)
APPROVED BY 0MB NO. 3150-0104 EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH (MNBB 7714), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON. DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104). OFFICE _OF MANAGEMENT AND BUDGET, WASHINGTON. DC 20503.
LER NUMBER (6)
PAGE C3l YEAR SEQUENTIAL NUMBER REVISION NUMBER SURRY POWER STATION, Unit 2 05000 - 281 96
-- 004 --
0 2 OF 5 TEXT (If more space is required. use additional copies of NRG Form 366A) (17) 1.0 DESCRIPTION OF THE EVENT On June_ 6, 1996, power escalation was in progress for Unit 2 upon completion of a scheduled refueling outage.
Reactor power was 16% based on Reactor Coolant System (RCS) [EIIS-AB] Loop delta T indications, and RCS average temperature was being controlled at 553 degrees-Fahrenheit using control rods in manual and Main Steam Dump Valves [EIIS-SB-TCV] in the steam pressure mode. The main Turbine [EIIS-TA] was rotating at 1800 rpm with turbine control in the operator automatic mode.
Preparations were being made to close the Main Generator [EIIS-TB] output breakers.
Between 2331 and 2333 hours0.027 days <br />0.648 hours <br />0.00386 weeks <br />8.877065e-4 months <br />, Control Room Operators were transferring from manual feedwater flow control with the Main Feedwater Regulation Valve (MFRV) [EIIS-SJ-ISV]
Bypass Valves to automatic feedwater control with the MFRVs. MFRVs A and C were opened first. Steam Generator (SG) [EIIS-AB-SG] water levels were oscillating in all three SGs. The Reactor Operator (RO) assigned to SGs A and B was stabilizing the level on SG A when he noticed SG B level increasing. MFRV B was verified closed, and the demand for the MFRV Bypass Valve B was lowered to reduce feedwater flow.
Level continued to increase, so deniand was lowered to fully close the MFRV B Bypass Valve. Level continued to increase.
At 2344 hours0.0271 days <br />0.651 hours <br />0.00388 weeks <br />8.91892e-4 months <br />, a high-high SG B level signal automatically tripped the running Main Feedwater Pump [EIIS-SJ-P] and the Main Turbine.
The turbine trip generated a reactor trip signal. The Reactor Protection System (RPS) actuated and functioned as designed, and all control rods inserted into the core.
The Motor-Driven Auxiliary Feedwater Pumps [EIIS-BA-P] automatically started as designed. Control Room Operators acted promptly to place the plant in a safe, hot shutdown condition in accordance with the proper. procedures. The Shift Technical Advisor calculated the shutdown margin and monitored the critical safety function status trees to verify that the unit conditions were acceptable. Individual Rod Position Indicator (IRPI) [EIIS-AA-ZI] F-8 initially indicated 13 steps then gradually drifted down to less than 10 steps.
The RCS cooled down below the 547 degree Fahrenheit (no load temperature) and reached a minimum of 539 degrees Fahrenheit.
RCS temperature subsequently stabilized at 547 degrees Fahrenheit after the Main Steam Dump Valves closed and the Auxiliary Feedwater (AFW) Pumps [EIIS-BA-P] were secured.
NRC FORM 366
/5-92)
. NUCLEAR REGULATORY COMMISSION LICENSING EVENT REPORT (LER}
(See reverse for required number of digits/characters for each block)
FACILITY NAME f1\\
DOCKET NUMBER 12\\
SURRY POWER STATION, Unit 2 05000 - 281 TEXT (If more space is required, use additional copies of NRG Form 366A) (17)
APPROVED BY 0MB NO. 3150-0104 EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH (MNBB 7714), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555*0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104). OFFICE OF MANAGEMENT AND BUDGET. WASHINGTON, DC 20503.
LER NUMBER (6)
PAGE (3)
YEAR SEQUENTIAL NUMBER REVISION NUMBER 96
0 3 OF 5 In accordance with 10 CFR 50.72(b)(2)(ii), a 4-hour non-emergency report to the Nuclear Regulatory Commission was made at 0325 hours0.00376 days <br />0.0903 hours <br />5.373677e-4 weeks <br />1.236625e-4 months <br /> due to the automatic RPS actuation. This event is being reported pursuant to 10 CFR 50.73(a)(2)(iv) due to automatic actuation of the RPS.
2.0 SIGNIFICANT SAFETY CONSEQUENCES AND IMPLICATIONS
Upon receipt of the reactor trip signal, the RPS actuated and functioned as designed, and all control rods inserted into the core. Control Room Operators acted promptly to place the plant in a safe, hot shutdown condition in accordance with the proper procedures.
The Shift Technical Advisor calculated the shutdown margin and monitored the critical safety function status trees to verify that the unit conditions were acceptable. Plant response was as expected and the unit stabilized at hot shutdown.
No conditions adverse to safety resulted from this event and the health and safety of the public were not affected.
3.0 CAUSE OF THE EVENT
The cause of the reactor trip was a high level in SG 8. This level swell occurred when the SG A stopped steaming and SG 8 picked up steam flow. This level swell combined with the initial level in the SG B caused the level to increase above the 75% high-high SG level trip setpoint. In response to increasing level in SG 8, the RO first lowered and then attempted to secure feedwater flow 30 seconds before the trip.
Investigations following the subsequent startup revealed that erratic Steam Dump Valve operation also contributed to the trip.
Several seconds of oscillating steam dump demand occurred at approximately 9 minutes and again at 3.5 minutes before the trip.
Steam Dump Valves 2-MS-TCV-205A and 8 oscillated in response to the demand signal. These steam dump oscillations increased the magnitude of the SG oscillations.
Also, a zero shift in the controller for 2-'FW-F9R-2558 MFRV Bypass Valve may have contributed to the level increase in SG 8.
The design of the Feedwater Control System requires manual operation of the MFRV Bypass Valve during startup. There are numerous variables involved in controlling SG levels; these variables along with the equipment malfunctions discussed in the previous paragraphs, resulted in the Control Room Operators being challenged to the point where SG level could not be successfully controlled.
u NRC FORM 366
,5-92)
. NUCLEAR REGULATORY COMMISSION LICENSING EVENT REPORT (LER)
(See reverse for required number of digits/characters for each block)
FACILITY NAME 11\\
DOCKET NUMBER 12\\
SURRY POWER STATION, Unit 2 05000 - 281 TEXT (If more space is required, use additional copies of NRG Form 366A) (17) 4.0 IMMEDIATE CORRECTIVE ACTION(S)
APPROVED BY 0MB NO. 3150-0104 EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH (MNBB 7714), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
LEA NUMBER 16\\
PAGE 13\\
YEAR SEQUENTIAL NUMBER REVISION NUMBER 96
0 4 OF 5 Following the trip, Control Room Operators acted promptly to place the plant in a safe, hot shutdown condition in accordance with the proper procedures. The Shift Technical Advisor calculated the shutdown margin and monitored the critical safety function status trees to verify that the unit conditions were acceptable.
Plant response was as expected and the unit stabilized at hot shutdown.
The SGs were initially fed by the AFW System and were later transferred to the MFRV Bypass Valves.
Decay heat was removed by the Main Steam Dump Valves discharging to the Main Condenser.
5.0 ADDITIONAL CORRECTIVE ACTION(S)
Investigations following the subsequent startup revealed that Steam Dump Valve operation was erratic while in the steam pressure mode.
This erratic operation occurred prior to the trip in the form of spikes in the demand to 2-MS-TCV-205A and B.
During power ascension on June 7, 1996, the steam dump valves were observed to modulate in response to RCS temperature changes. Subsequent investigation by l&C determined that both RCS average temperature and steam pressure voltages were being fed to the valves due to a faulty relay in the steam dump control system. This relay was replaced. The steam dump valves were tested in both the RCS average temperature and steam pressure modes with satisfactory results.
During startup, MFRV Bypass Valve 2-FW-FCV-255B was noted as requiring less demand than the MFRV Bypass Valve A to provide the same flow (e.g., 60% demand on MFRV B provided the same flow as 80% demand on MFRV A). The demand was lowered to zero for MFRV B Bypass Valve in order to isolate feedwater flow to the SG B but level continued to increase. Following the trip, l&C technicians determined that the valve was not going fully closed on demand; however, when instrument air to the positioner was isolated, the valve would move further in the closed direction. Further investigation determined a
slightly elevated pneumatic output from the Electric/Pneumatic (E/P) transducer.
When the cover was removed from the E/P transducer, the input signal wires were found lying against the force beam causing elevated pneumatic output. The wires were relocated away from the force beam and the valve fully closed with E/P input at its minimum.
" rr==N=:=R===c""=F===o===R=M=3=66=========1
.S. NUCLEAR REGULATORY COMMISSION APPROVED BY 0MB NO. 3150-0104 EXPIRES 5/31/95 I
f (5-92)
LICENSING EVENT REPORT (LER)
(See reverse for required number of digits/characters for each block)
FACILITY NAME (1)
DOCKET NUMBER (2)
ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH (MNBB 7714), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
LER NUMBER !6l YEAR SEQUENTIAL NUMBER REVISION NUMBER PAGE(3l SURRY POWER STATION, Unit 2 05000 - 281 96
-- 004 --
0 5oF5 TEXT (If more space is required, use additional copies of NRG Form 366A) (17)
Further investigation of the MFRV Bypass Valve leakage and the Steam Dump Valve erratic operation is ongoing. Further corrective action related to these items may be recommended as a result of this investigation and will be tracked by the corrective action process.
A calibration check was performed on IRPI F-8 and it was found to be indicating high.
IRPI F-8 was adjusted satisfactorily.
6.0 ACTIONS TO PREVENT RECURRENCE None.
7.0 SIMILAR EVENTS
LER S2-86-003 - Turbine trip/reactor trip from high SG Level due to MFRV bypass valve failing to close on demand
8.0 ADDITIONAL INFORMATION
Unit 1 was operating at 100% during this event.
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05000280/LER-1996-001, :on 951213,ESW Pump Was Inoperable Due to Loss of Missile Protection for Piping.Revised DCP 91-025 |
- on 951213,ESW Pump Was Inoperable Due to Loss of Missile Protection for Piping.Revised DCP 91-025
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii)(A) | 05000281/LER-1996-001-02, :on 960222,through-wall Leak Identified in Unit 2 RHR Piping.Caused by General Intergranular Attack on Inside Surface of Piping.Conservative Leakage Rate of One Drop Every Ten Minutes Estimated |
- on 960222,through-wall Leak Identified in Unit 2 RHR Piping.Caused by General Intergranular Attack on Inside Surface of Piping.Conservative Leakage Rate of One Drop Every Ten Minutes Estimated
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii)(A) | 05000280/LER-1996-002-01, :on 960303,containment Isolation Valve Inoperable.Caused by Personnel Error.C/A:Individuals Counseled |
- on 960303,containment Isolation Valve Inoperable.Caused by Personnel Error.C/A:Individuals Counseled
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | 05000281/LER-1996-002-02, :on 960408,EDG Fire Suppression Sys Declared Inoperable Due to Personnel Error.Submitted Station Deviation Rept |
- on 960408,EDG Fire Suppression Sys Declared Inoperable Due to Personnel Error.Submitted Station Deviation Rept
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | 05000281/LER-1996-003-01, :on 960512,Unit 2 Pressurizer Safety Valve as Found Lift Setting Out of Tolerance.Valve Was Reassembled & Lift Setting Was Established & Tested Satisfactorily |
- on 960512,Unit 2 Pressurizer Safety Valve as Found Lift Setting Out of Tolerance.Valve Was Reassembled & Lift Setting Was Established & Tested Satisfactorily
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii)(A) | 05000280/LER-1996-003-02, :on 960513,control Room Air Handling Units (AHU) Declared Inoperable.Caused by Mechanical Failure. Adjusted 1-VS-AC-2 Backdraft Dampers Counterweight Arm for AHU 1-VS-AC-2 |
- on 960513,control Room Air Handling Units (AHU) Declared Inoperable.Caused by Mechanical Failure. Adjusted 1-VS-AC-2 Backdraft Dampers Counterweight Arm for AHU 1-VS-AC-2
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | 05000280/LER-1996-004, :on 960510,noticed That Hydrogen Analyzers Inoperable.Caused by Procedural Deficiencies Due to Personnel Error.Permanent Changes to Hydrogen Analyzer Instrument Calibr Procedures Implemented |
- on 960510,noticed That Hydrogen Analyzers Inoperable.Caused by Procedural Deficiencies Due to Personnel Error.Permanent Changes to Hydrogen Analyzer Instrument Calibr Procedures Implemented
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | 05000281/LER-1996-004-02, :on 960606,turbine/reactor Trip Occurred.Caused by High Level in Steam Generator B.Placed Plant in Hot Shutdown Condition,Calculated Shutdown Margin & Monitored Critical Safety Function Status Trees |
- on 960606,turbine/reactor Trip Occurred.Caused by High Level in Steam Generator B.Placed Plant in Hot Shutdown Condition,Calculated Shutdown Margin & Monitored Critical Safety Function Status Trees
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | 05000280/LER-1996-005, :on 960506,charging Pumps Declared Inoperable. Caused by Air Entering Service Water Sys Through Valve 2-SW-MOV-201B.Personnel Closed Valve 2SW-MOV-201B |
- on 960506,charging Pumps Declared Inoperable. Caused by Air Entering Service Water Sys Through Valve 2-SW-MOV-201B.Personnel Closed Valve 2SW-MOV-201B
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii)(B) | 05000281/LER-1996-005-01, :on 960803,manual Reactor Trip.Caused by Loss of Electro Hydraulic Control Pressure.Repaired Two Compression Fitting Union Connections on Leaking Fitting & Performed Evaluations on Other Tubing |
- on 960803,manual Reactor Trip.Caused by Loss of Electro Hydraulic Control Pressure.Repaired Two Compression Fitting Union Connections on Leaking Fitting & Performed Evaluations on Other Tubing
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2) | 05000280/LER-1996-006, :on 960618,anti-corrosion Coating Had Not Been Reapplied to Station Battery 2B.Caused by Procedural Error in That Verbatim TS Compliance Not Reflected in Procedures. Coating Was Applied to Batteries |
- on 960618,anti-corrosion Coating Had Not Been Reapplied to Station Battery 2B.Caused by Procedural Error in That Verbatim TS Compliance Not Reflected in Procedures. Coating Was Applied to Batteries
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(x) | 05000280/LER-1996-007, :on 960821,failed to Complete Fire Detection Zone Inspections within Required Time Period.Caused by Personnel Error.Counseled Personnel Re Fire Detection Zone Inspections & Revised Fire Watch Training |
- on 960821,failed to Complete Fire Detection Zone Inspections within Required Time Period.Caused by Personnel Error.Counseled Personnel Re Fire Detection Zone Inspections & Revised Fire Watch Training
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | 05000280/LER-1996-008-01, :on 961112,water Gas Decay Tank Oxygen Analyzer Pressure Sensors Inoperable Due to Vendor Supplied Equipment Not Meeting Procurement specifications.Post-implementation Procedures Revised & Transducers Replaced |
- on 961112,water Gas Decay Tank Oxygen Analyzer Pressure Sensors Inoperable Due to Vendor Supplied Equipment Not Meeting Procurement specifications.Post-implementation Procedures Revised & Transducers Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) |
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