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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18152B4411999-08-27027 August 1999 LER 99-005-00:on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed ML18152B4421999-08-27027 August 1999 LER 99-006-00:on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With 990827 Ltr ML18152B3771999-08-13013 August 1999 LER 99-004-00:on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms ML18152B4181999-05-18018 May 1999 LER 99-002-00:on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With 990518 Ltr ML18152B4111999-04-28028 April 1999 LER 99-003-00:on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With 990428 Ltr ML18153A2741999-03-29029 March 1999 LER 99-002-00:on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212 ML18153A2681999-03-19019 March 1999 LER 98-013-01:on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr ML18152B7261999-01-21021 January 1999 LER 99-001-00:on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable ML18152B5811998-12-16016 December 1998 LER 98-013-00:on 981122,turbine/reactor Trip on High SG Level Occurred.Caused by Instrument Failure.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B5781998-12-16016 December 1998 LER 98-014-00:on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B7121998-12-0404 December 1998 LER 98-S01-00:on 981105,noted Failure to Deactivate Station Access Badge.Caused by Human Error.Licensee Will Now Deactivate Station Badges Before Clearance Is Revoked & Process for Badge Deactivations Have Been Strengthened ML18152B7041998-12-0101 December 1998 LER 98-012-00:on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With 981201 Ltr ML18152B6161998-11-0606 November 1998 LER 98-011-00:on 981008,diesel Driven Fire Pump Failed to Start During Performance of Monthly Operability Test.Caused by Faulty Overspeed Trip Device Failure.Diesel Driven Fire Pump Declared Inoperable ML18152B6081998-10-23023 October 1998 LER 98-010-01:on 980715,intake Canal Level Probes Were Inoperable Due to Marine Growth.Caused by Design of Canal Level Instrumentation.Canal Level Probes Will Continue to Be Monitored More Closely ML18152B7811998-07-31031 July 1998 LER 98-010-00:on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status ML18153A2581998-06-0303 June 1998 LER 98-009-00:on 980509,nonisolable Leak of Reactor Coolant Pump Seal Injection Line Weld,Was Discovered.Caused by Lack of Fusion or Thermal Fatigue Coupled W/Vibration Stress Due to Loose Rod Hanger.Rcp Seal Injection Line Removed ML18152B8241998-05-22022 May 1998 LER 98-008-00:on 980228,auxiliary Ventilation Fans Were Noted in Condition Outside of Design Basis.Caused by Failure to Recognize Potential Impact of Certain Design Basis Accident Scenarios.No Corrective Actions Needed ML18152B7951998-04-29029 April 1998 LER 98-007-00:on 980330,radiation Monitors Were Declared Inoperable.Caused by Change in Operating Temperature Range. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-6 ML18153A2521998-04-22022 April 1998 LER 98-005-01:on 980212,fire Watch Insp Exceeded One Hour. Caused by Lack of Attention to Detail by Individual Involved.Individual Involved Was Coached on Requirement to Perform Fire Watch Patrols within Required Time Frame ML18153A2511998-04-22022 April 1998 LER 98-006-00:on 980324,unisolable Through Wall Leak of RCP Thermowell Was Noted.Cause of Leak Is Unknown.Rtd Will Be Replaced ML18153A2391998-03-13013 March 1998 LER 98-005-00:on 980212,fire Watch Insp Frequency Exceeded One H Occurred.Category 2 Root Cause Evaluation Being Conducted to Determine Cause of Event.Station Deviation Issued ML18153A2341998-03-0909 March 1998 LER 98-003-00:on 980226,no Procedural Guidance for Maintaining EDG Minimum Fuel Supply During Loop,Was Identified.Caused by Absence of Procedural Instructions. Deviation Rept Submitted to Document Deviating Condition ML18153A2301998-03-0606 March 1998 LER 98-004-00:on 980206,fire Watch Was Released Prematurely Resulting in Violation of Ts.Caused by Inadequate Planning of Repair Activity.Work Orders Will Include Ref to Applicable Procedures Developed to Assist in Repairs ML18153A2251998-03-0404 March 1998 LER 98-002-00:on 980202,automatic Turbine Trip Resulted in Automatic Reactor Trip.Caused Degraded Generator Voltage Regulator sub-component Failure.Placed Plant in Safe Hot SD & Replaced Intermittent Relay & Relay Socket ML18153A2201998-02-0606 February 1998 LER 98-001-00:on 980108,deficient Test Due to Faulty Test Equipment Resulted in TS Violation.Caused by Faulty Vibration Analyzer Cable or Loose Connection.Station Deviation Rept Was submitted.W/980206 Ltr ML18153A2071998-01-13013 January 1998 LER 97-012-01:on 971028,loss of Power to Latching Mechanism on Several Doors Occurred.Caused by Tripping of Two Breakers in Security Distribution Panel.Reset Affected Breakers Which Restored Power to Security Systems & Affected Doors ML18153A2101998-01-13013 January 1998 LER 97-009-01:on 971014,declared Intake Canal Level Probes Inoperable Due to Marine Growth.Caused by Inadequate Maint of Intake Canal Level Probes.Subject Probes Were Cleaned, Tested Satisfactorily & Returned to Operable Status ML18153A1911997-11-26026 November 1997 LER 97-011-00:on 971030,determined That Periodic Test Procedures for Testing Reactor Trip Bypass Breakers Did Not Test Manual Undervoltage Trip.Caused by mis-interpretation of Term in-service. Procedures Revised ML18153A1971997-11-26026 November 1997 LER 97-012-00:on 971028,loss of Power to Latching Mechanism on Several Doors Occurred.Caused by Tripping of Breaker in Security Distribution Panel in Central Alarm Station (CAS) Panel.Breakers in Affected CAS Panel Reset ML18153A1921997-11-25025 November 1997 LER 97-010-00:on 971028,discovered Missed Fire Protection Surveillance Pt.Caused by Personnel Error.Satisfactorily Completed PT Procedure 0-OPT-FP-009 & Diesel Driven Fire Pump 1-FP-P-2 Declared operable.W/971125 Ltr ML18153A1831997-11-12012 November 1997 LER 97-009-00:on 971014,declared Intake Canal Level Probes Inoperable Due to Marine Growth.Cause Indeterminate.Divers Inspected,Cleaned & Returned Probes to Operable Status & Initiated Interdepartmental Team to Investigate Cause ML18153A1791997-11-0707 November 1997 LER 97-008-00:on 971011,invalid Actuation of ESF Occurred. Caused by Personnel Errors.Main CR Bottled Air Sys Isolated & Containment Hydrogen Analyzer Heat Tracing Actuation Signal Reset ML18153A1721997-10-30030 October 1997 LER 97-007-00:on 970930,determined That Plant Was Outside App R Design Basis Due to Vital Bus Isolation Issue.Caused by Personnel Error.Installed Circuit Protective Device During Oct 1997 Refueling Outage ML18153A1421997-06-10010 June 1997 LER 97-001-01:on 970123,shutdown Occurred Due to Drain Line Weld Leak.Inspected & Tested Turbine Trip Actuation circuitry.W/970610 Ltr ML18153A1391997-05-28028 May 1997 LER 97-005-00:on 970502,Unit 1 Power Range Nuclear Instrumentation Was Inoperable Due to Personnel Error.Sro & STA That Were Involved in Event Were Counseled ML18153A1291997-04-18018 April 1997 LER 97-006-00:on 970320,loss of Refueling Integrity Due to Inadequate Containment Closure Process & Verification.Fuel Movement Stopped IAW Action Statement Requirements of TS 3.10.B.W/970418 Ltr ML18153A1281997-04-15015 April 1997 LER 97-004-00:on 970317,main Steam Safety Valve Was Outside as Found Setpoint Tolerance.Specific Cause Unknown,However, Minor Setpoint Drift Can Be Expected.No Immediate Corrective Actions performed.W/970415 Ltr ML18153A1241997-04-0808 April 1997 LER 97-002-01:on 970116,one Train of Auxiliary Ventilation Sys Was Inoperable Outside of Ts.Caused by Personnel Error. Submitted Deviation Rept Re Reverse Rotation of Fan & Work Request to Adjust linkage.W/970408 Ltr ML18153A1191997-03-19019 March 1997 LER 97-001-00:on 970218,manual Reactor Trip & ESF Actuation Occurred Due to Loss of EHC Control Power.Caused by Momentary Short.Relay Card Was replaced.W/970319 Ltr ML18153A1201997-03-19019 March 1997 LER 97-003-00:on 970219,loss of Pressurizer Heaters Resulted in Manual U1 Trip & U2 ESF Actuation.Caused by Loss of Group C Pressurizer Proportional Heaters.Reactor Trip Breakers Were Verified open.W/970319 Ltr ML18153A1131997-02-20020 February 1997 LER 97-001-00:on 970123,shutdown Occurred Due to Steam Drain Line Weld Leak.Management Was Notified & Shift Supervisor Invoked Requirements of TS 4.15.C.1.W/undtd Ltr ML18153A1101997-02-13013 February 1997 LER 97-002-00:on 970116,one Train of Auxiliary Ventilation Sys Declared Inoperable.Caused by Personnel Error.Properly Adjusted Damper 1-VS-MOD-58B & Exited Seven Day LCO on 970116.W/970214 Ltr ML18153A0951997-01-0202 January 1997 LER 97-002-00:on 961213,automatic Reactor Trip Occurred During Planned Shutdown.Caused by Steam Flow/Feedwater Flow Mismatch.Rps Functioned as Designed & Plant Placed in Hot Shutdown ML18153A0931996-12-12012 December 1996 LER 96-008-00:on 961112,water Gas Decay Tank Oxygen Analyzer Pressure Sensors Inoperable Due to Vendor Supplied Equipment Not Meeting Procurement specifications.Post-implementation Procedures Revised & Transducers replaced.W/961212 Ltr ML18153A0691996-09-19019 September 1996 LER 96-007-00:on 960821,failed to Complete Fire Detection Zone Inspections within Required Time Period.Caused by Personnel Error.Counseled Personnel Re Fire Detection Zone Inspections & Revised Fire Watch training.W/960920 Ltr ML18153A0481996-08-26026 August 1996 LER 96-005-00:on 960803,manual Reactor Trip.Caused by Loss of Electro Hydraulic Control Pressure.Repaired Two Compression Fitting Union Connections on Leaking Fitting & Performed Evaluations on Other tubing.W/960826 Ltr ML18153A0521996-08-20020 August 1996 LER 96-004-01:on 960510,discovered Hydrogen Analyzers Inoperable.Caused by Procedural Deficiencies.Implemented Permanent Changes to Hydrogen Analyzer Instrument Calibr Procedures.W/960820 Ltr ML18153A0321996-07-30030 July 1996 LER 96-006-01:on 960618,anti-corrosion Coating Had Not Been Reapplied to Station Battery 2B.Caused by Procedural Error in That Verbatim TS Compliance Not Reflected in Procedures. Coating Was Applied to batteries.W/960730 Ltr ML18153A0281996-07-17017 July 1996 LER 96-006-00:on 960618,failed to Apply anti-corrosion Coating to Station Battery 2B.Caused by Procedural Error. Applied anti-corrosion Coating to Batteries & Revised TS 4.6.C.1.f Re Battery Coating requirements.W/960717 Ltr ML18153A0141996-07-0202 July 1996 LER 96-004-00:on 960606,turbine/reactor Trip Occurred.Caused by High Level in Steam Generator B.Placed Plant in Hot Shutdown Condition,Calculated Shutdown Margin & Monitored Critical Safety Function Status trees.W/960702 Ltr 1999-08-27
[Table view] Category:RO)
MONTHYEARML18152B4411999-08-27027 August 1999 LER 99-005-00:on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed ML18152B4421999-08-27027 August 1999 LER 99-006-00:on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With 990827 Ltr ML18152B3771999-08-13013 August 1999 LER 99-004-00:on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms ML18152B4181999-05-18018 May 1999 LER 99-002-00:on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With 990518 Ltr ML18152B4111999-04-28028 April 1999 LER 99-003-00:on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With 990428 Ltr ML18153A2741999-03-29029 March 1999 LER 99-002-00:on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212 ML18153A2681999-03-19019 March 1999 LER 98-013-01:on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr ML18152B7261999-01-21021 January 1999 LER 99-001-00:on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable ML18152B5811998-12-16016 December 1998 LER 98-013-00:on 981122,turbine/reactor Trip on High SG Level Occurred.Caused by Instrument Failure.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B5781998-12-16016 December 1998 LER 98-014-00:on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B7121998-12-0404 December 1998 LER 98-S01-00:on 981105,noted Failure to Deactivate Station Access Badge.Caused by Human Error.Licensee Will Now Deactivate Station Badges Before Clearance Is Revoked & Process for Badge Deactivations Have Been Strengthened ML18152B7041998-12-0101 December 1998 LER 98-012-00:on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With 981201 Ltr ML18152B6161998-11-0606 November 1998 LER 98-011-00:on 981008,diesel Driven Fire Pump Failed to Start During Performance of Monthly Operability Test.Caused by Faulty Overspeed Trip Device Failure.Diesel Driven Fire Pump Declared Inoperable ML18152B6081998-10-23023 October 1998 LER 98-010-01:on 980715,intake Canal Level Probes Were Inoperable Due to Marine Growth.Caused by Design of Canal Level Instrumentation.Canal Level Probes Will Continue to Be Monitored More Closely ML18152B7811998-07-31031 July 1998 LER 98-010-00:on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status ML18153A2581998-06-0303 June 1998 LER 98-009-00:on 980509,nonisolable Leak of Reactor Coolant Pump Seal Injection Line Weld,Was Discovered.Caused by Lack of Fusion or Thermal Fatigue Coupled W/Vibration Stress Due to Loose Rod Hanger.Rcp Seal Injection Line Removed ML18152B8241998-05-22022 May 1998 LER 98-008-00:on 980228,auxiliary Ventilation Fans Were Noted in Condition Outside of Design Basis.Caused by Failure to Recognize Potential Impact of Certain Design Basis Accident Scenarios.No Corrective Actions Needed ML18152B7951998-04-29029 April 1998 LER 98-007-00:on 980330,radiation Monitors Were Declared Inoperable.Caused by Change in Operating Temperature Range. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-6 ML18153A2521998-04-22022 April 1998 LER 98-005-01:on 980212,fire Watch Insp Exceeded One Hour. Caused by Lack of Attention to Detail by Individual Involved.Individual Involved Was Coached on Requirement to Perform Fire Watch Patrols within Required Time Frame ML18153A2511998-04-22022 April 1998 LER 98-006-00:on 980324,unisolable Through Wall Leak of RCP Thermowell Was Noted.Cause of Leak Is Unknown.Rtd Will Be Replaced ML18153A2391998-03-13013 March 1998 LER 98-005-00:on 980212,fire Watch Insp Frequency Exceeded One H Occurred.Category 2 Root Cause Evaluation Being Conducted to Determine Cause of Event.Station Deviation Issued ML18153A2341998-03-0909 March 1998 LER 98-003-00:on 980226,no Procedural Guidance for Maintaining EDG Minimum Fuel Supply During Loop,Was Identified.Caused by Absence of Procedural Instructions. Deviation Rept Submitted to Document Deviating Condition ML18153A2301998-03-0606 March 1998 LER 98-004-00:on 980206,fire Watch Was Released Prematurely Resulting in Violation of Ts.Caused by Inadequate Planning of Repair Activity.Work Orders Will Include Ref to Applicable Procedures Developed to Assist in Repairs ML18153A2251998-03-0404 March 1998 LER 98-002-00:on 980202,automatic Turbine Trip Resulted in Automatic Reactor Trip.Caused Degraded Generator Voltage Regulator sub-component Failure.Placed Plant in Safe Hot SD & Replaced Intermittent Relay & Relay Socket ML18153A2201998-02-0606 February 1998 LER 98-001-00:on 980108,deficient Test Due to Faulty Test Equipment Resulted in TS Violation.Caused by Faulty Vibration Analyzer Cable or Loose Connection.Station Deviation Rept Was submitted.W/980206 Ltr ML18153A2071998-01-13013 January 1998 LER 97-012-01:on 971028,loss of Power to Latching Mechanism on Several Doors Occurred.Caused by Tripping of Two Breakers in Security Distribution Panel.Reset Affected Breakers Which Restored Power to Security Systems & Affected Doors ML18153A2101998-01-13013 January 1998 LER 97-009-01:on 971014,declared Intake Canal Level Probes Inoperable Due to Marine Growth.Caused by Inadequate Maint of Intake Canal Level Probes.Subject Probes Were Cleaned, Tested Satisfactorily & Returned to Operable Status ML18153A1911997-11-26026 November 1997 LER 97-011-00:on 971030,determined That Periodic Test Procedures for Testing Reactor Trip Bypass Breakers Did Not Test Manual Undervoltage Trip.Caused by mis-interpretation of Term in-service. Procedures Revised ML18153A1971997-11-26026 November 1997 LER 97-012-00:on 971028,loss of Power to Latching Mechanism on Several Doors Occurred.Caused by Tripping of Breaker in Security Distribution Panel in Central Alarm Station (CAS) Panel.Breakers in Affected CAS Panel Reset ML18153A1921997-11-25025 November 1997 LER 97-010-00:on 971028,discovered Missed Fire Protection Surveillance Pt.Caused by Personnel Error.Satisfactorily Completed PT Procedure 0-OPT-FP-009 & Diesel Driven Fire Pump 1-FP-P-2 Declared operable.W/971125 Ltr ML18153A1831997-11-12012 November 1997 LER 97-009-00:on 971014,declared Intake Canal Level Probes Inoperable Due to Marine Growth.Cause Indeterminate.Divers Inspected,Cleaned & Returned Probes to Operable Status & Initiated Interdepartmental Team to Investigate Cause ML18153A1791997-11-0707 November 1997 LER 97-008-00:on 971011,invalid Actuation of ESF Occurred. Caused by Personnel Errors.Main CR Bottled Air Sys Isolated & Containment Hydrogen Analyzer Heat Tracing Actuation Signal Reset ML18153A1721997-10-30030 October 1997 LER 97-007-00:on 970930,determined That Plant Was Outside App R Design Basis Due to Vital Bus Isolation Issue.Caused by Personnel Error.Installed Circuit Protective Device During Oct 1997 Refueling Outage ML18153A1421997-06-10010 June 1997 LER 97-001-01:on 970123,shutdown Occurred Due to Drain Line Weld Leak.Inspected & Tested Turbine Trip Actuation circuitry.W/970610 Ltr ML18153A1391997-05-28028 May 1997 LER 97-005-00:on 970502,Unit 1 Power Range Nuclear Instrumentation Was Inoperable Due to Personnel Error.Sro & STA That Were Involved in Event Were Counseled ML18153A1291997-04-18018 April 1997 LER 97-006-00:on 970320,loss of Refueling Integrity Due to Inadequate Containment Closure Process & Verification.Fuel Movement Stopped IAW Action Statement Requirements of TS 3.10.B.W/970418 Ltr ML18153A1281997-04-15015 April 1997 LER 97-004-00:on 970317,main Steam Safety Valve Was Outside as Found Setpoint Tolerance.Specific Cause Unknown,However, Minor Setpoint Drift Can Be Expected.No Immediate Corrective Actions performed.W/970415 Ltr ML18153A1241997-04-0808 April 1997 LER 97-002-01:on 970116,one Train of Auxiliary Ventilation Sys Was Inoperable Outside of Ts.Caused by Personnel Error. Submitted Deviation Rept Re Reverse Rotation of Fan & Work Request to Adjust linkage.W/970408 Ltr ML18153A1191997-03-19019 March 1997 LER 97-001-00:on 970218,manual Reactor Trip & ESF Actuation Occurred Due to Loss of EHC Control Power.Caused by Momentary Short.Relay Card Was replaced.W/970319 Ltr ML18153A1201997-03-19019 March 1997 LER 97-003-00:on 970219,loss of Pressurizer Heaters Resulted in Manual U1 Trip & U2 ESF Actuation.Caused by Loss of Group C Pressurizer Proportional Heaters.Reactor Trip Breakers Were Verified open.W/970319 Ltr ML18153A1131997-02-20020 February 1997 LER 97-001-00:on 970123,shutdown Occurred Due to Steam Drain Line Weld Leak.Management Was Notified & Shift Supervisor Invoked Requirements of TS 4.15.C.1.W/undtd Ltr ML18153A1101997-02-13013 February 1997 LER 97-002-00:on 970116,one Train of Auxiliary Ventilation Sys Declared Inoperable.Caused by Personnel Error.Properly Adjusted Damper 1-VS-MOD-58B & Exited Seven Day LCO on 970116.W/970214 Ltr ML18153A0951997-01-0202 January 1997 LER 97-002-00:on 961213,automatic Reactor Trip Occurred During Planned Shutdown.Caused by Steam Flow/Feedwater Flow Mismatch.Rps Functioned as Designed & Plant Placed in Hot Shutdown ML18153A0931996-12-12012 December 1996 LER 96-008-00:on 961112,water Gas Decay Tank Oxygen Analyzer Pressure Sensors Inoperable Due to Vendor Supplied Equipment Not Meeting Procurement specifications.Post-implementation Procedures Revised & Transducers replaced.W/961212 Ltr ML18153A0691996-09-19019 September 1996 LER 96-007-00:on 960821,failed to Complete Fire Detection Zone Inspections within Required Time Period.Caused by Personnel Error.Counseled Personnel Re Fire Detection Zone Inspections & Revised Fire Watch training.W/960920 Ltr ML18153A0481996-08-26026 August 1996 LER 96-005-00:on 960803,manual Reactor Trip.Caused by Loss of Electro Hydraulic Control Pressure.Repaired Two Compression Fitting Union Connections on Leaking Fitting & Performed Evaluations on Other tubing.W/960826 Ltr ML18153A0521996-08-20020 August 1996 LER 96-004-01:on 960510,discovered Hydrogen Analyzers Inoperable.Caused by Procedural Deficiencies.Implemented Permanent Changes to Hydrogen Analyzer Instrument Calibr Procedures.W/960820 Ltr ML18153A0321996-07-30030 July 1996 LER 96-006-01:on 960618,anti-corrosion Coating Had Not Been Reapplied to Station Battery 2B.Caused by Procedural Error in That Verbatim TS Compliance Not Reflected in Procedures. Coating Was Applied to batteries.W/960730 Ltr ML18153A0281996-07-17017 July 1996 LER 96-006-00:on 960618,failed to Apply anti-corrosion Coating to Station Battery 2B.Caused by Procedural Error. Applied anti-corrosion Coating to Batteries & Revised TS 4.6.C.1.f Re Battery Coating requirements.W/960717 Ltr ML18153A0141996-07-0202 July 1996 LER 96-004-00:on 960606,turbine/reactor Trip Occurred.Caused by High Level in Steam Generator B.Placed Plant in Hot Shutdown Condition,Calculated Shutdown Margin & Monitored Critical Safety Function Status trees.W/960702 Ltr 1999-08-27
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18152A2811999-10-12012 October 1999 Technical Basis for Elimination of Nozzle Inner Radius Insps (for Nozzles Other than Reactor Vessel),Technical Basis for ASME Section XI Code Case N-619. ML18152B3531999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Surry Power Station,Units 1 & 2.With 991012 Ltr ML18152B6651999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Surry Power Station Units 1 & 2.With 990915 Ltr ML18152B4421999-08-27027 August 1999 LER 99-006-00:on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With 990827 Ltr ML18152B4411999-08-27027 August 1999 LER 99-005-00:on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed ML18151A3981999-08-13013 August 1999 SPS Unit 2 ISI Summary Rept for 1999 Refueling Outage. ML18152B3771999-08-13013 August 1999 LER 99-004-00:on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms ML18152B3791999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Surry Power Station,Units 1 & 2.With 990811 Ltr ML18152B3911999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Surry Power Station,Units 1 & 2.With 990713 Ltr ML18152B4341999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Surry Power Station,Units 1 & 2.With 990614 Ltr ML20195E2401999-05-31031 May 1999 Rev 2 to COLR for SPS Unit 2 Cycle 16 Pattern Ag ML18152B4181999-05-18018 May 1999 LER 99-002-00:on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With 990518 Ltr ML18152B4161999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Surry Power Station Units 1 & 2.With 990512 Ltr ML18152B4111999-04-28028 April 1999 LER 99-003-00:on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With 990428 Ltr ML18152B6511999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Surry Power Station Units 1 & 2 ML18153A2741999-03-29029 March 1999 LER 99-002-00:on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212 ML18153A2681999-03-19019 March 1999 LER 98-013-01:on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr ML18152B7331999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Surry Power Station,Units 1 & 2.With 990310 Ltr ML18152B5421999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Surry Power Station,Units 1 & 2.With 990210 Ltr ML18151A3031999-01-29029 January 1999 ISI Summary Rept for 1998 Refueling Outage,Including Form NIS-1, Owners Rept for ISIs & Form NIS-2, Owners Rept for Repairs & Replacements. ML18152B7261999-01-21021 January 1999 LER 99-001-00:on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable ML18152B6011998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Surry Power Station,Units 1 & 2.With 990115 Ltr ML18152B5781998-12-16016 December 1998 LER 98-014-00:on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B5811998-12-16016 December 1998 LER 98-013-00:on 981122,turbine/reactor Trip on High SG Level Occurred.Caused by Instrument Failure.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B7121998-12-0404 December 1998 LER 98-S01-00:on 981105,noted Failure to Deactivate Station Access Badge.Caused by Human Error.Licensee Will Now Deactivate Station Badges Before Clearance Is Revoked & Process for Badge Deactivations Have Been Strengthened ML18152B7041998-12-0101 December 1998 LER 98-012-00:on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With 981201 Ltr ML18152B7081998-11-30030 November 1998 Rev 0 to COLR for Surry 1 Cycle 16,Pattern Un. ML18152B5721998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Surry Power Station,Units 1 & 2.With 981214 Ltr ML18152B6161998-11-0606 November 1998 LER 98-011-00:on 981008,diesel Driven Fire Pump Failed to Start During Performance of Monthly Operability Test.Caused by Faulty Overspeed Trip Device Failure.Diesel Driven Fire Pump Declared Inoperable ML18152B6241998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Surry Power Station Units 1 & 2.With 981111 Ltr ML18152B6081998-10-23023 October 1998 LER 98-010-01:on 980715,intake Canal Level Probes Were Inoperable Due to Marine Growth.Caused by Design of Canal Level Instrumentation.Canal Level Probes Will Continue to Be Monitored More Closely ML18152B6881998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Surry Power Station Units 1 & 2.With 981012 Ltr ML18153A3271998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Surry Power Station,Units 1 & 2 ML18152B7811998-07-31031 July 1998 LER 98-010-00:on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status ML18153A3161998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Surry Power Station Units 1 & 2.W/980807 Ltr ML18152B7621998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Surry Power Station,Units 1 & 2.W/980707 Ltr ML18153A2581998-06-0303 June 1998 LER 98-009-00:on 980509,nonisolable Leak of Reactor Coolant Pump Seal Injection Line Weld,Was Discovered.Caused by Lack of Fusion or Thermal Fatigue Coupled W/Vibration Stress Due to Loose Rod Hanger.Rcp Seal Injection Line Removed ML20248F7441998-05-31031 May 1998 Reactor Vessel Working Group,Response to RAI Regarding Reactor Pressure Vessel Integrity ML18153A3141998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Surry Power Station,Units 1 & 2.W/980610 ML18152B8241998-05-22022 May 1998 LER 98-008-00:on 980228,auxiliary Ventilation Fans Were Noted in Condition Outside of Design Basis.Caused by Failure to Recognize Potential Impact of Certain Design Basis Accident Scenarios.No Corrective Actions Needed ML18152B8161998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Surry Power Station Units 1 & 2.W/980508 Ltr ML18152B7951998-04-29029 April 1998 LER 98-007-00:on 980330,radiation Monitors Were Declared Inoperable.Caused by Change in Operating Temperature Range. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-6 ML18153A2511998-04-22022 April 1998 LER 98-006-00:on 980324,unisolable Through Wall Leak of RCP Thermowell Was Noted.Cause of Leak Is Unknown.Rtd Will Be Replaced ML18153A2521998-04-22022 April 1998 LER 98-005-01:on 980212,fire Watch Insp Exceeded One Hour. Caused by Lack of Attention to Detail by Individual Involved.Individual Involved Was Coached on Requirement to Perform Fire Watch Patrols within Required Time Frame ML20217P9941998-04-0707 April 1998 Safety Evaluation Granting Licensee Third 10-yr Inservice Insp Program Relief Requests SR-018 - Sr-024 ML18153A2951998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Sps,Units 1 & 2.W/ 980408 Ltr ML18153A2391998-03-13013 March 1998 LER 98-005-00:on 980212,fire Watch Insp Frequency Exceeded One H Occurred.Category 2 Root Cause Evaluation Being Conducted to Determine Cause of Event.Station Deviation Issued ML18153A2341998-03-0909 March 1998 LER 98-003-00:on 980226,no Procedural Guidance for Maintaining EDG Minimum Fuel Supply During Loop,Was Identified.Caused by Absence of Procedural Instructions. Deviation Rept Submitted to Document Deviating Condition ML18153A2301998-03-0606 March 1998 LER 98-004-00:on 980206,fire Watch Was Released Prematurely Resulting in Violation of Ts.Caused by Inadequate Planning of Repair Activity.Work Orders Will Include Ref to Applicable Procedures Developed to Assist in Repairs ML18153A2251998-03-0404 March 1998 LER 98-002-00:on 980202,automatic Turbine Trip Resulted in Automatic Reactor Trip.Caused Degraded Generator Voltage Regulator sub-component Failure.Placed Plant in Safe Hot SD & Replaced Intermittent Relay & Relay Socket 1999-09-30
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- 10CFR50.73 Virginia Electric and Power Company Surry Power Station 5570 Hog Island Road JUNE 10, 1997 Surry, Virginia 23883 U.S. Nuclear Regulatory Commission Serial No.: 97-101 A Document Control Desk SPS:mdk Washington, D. C. 20555 Docket No.: 50-280 License No.: DPR-32
Dear Sirs:
Pursuant to Surry Power Station Technical Specifications, Virginia Electric and Power Company hereby submits the following updated Licensee Event Report applicable to Surry Power Station Unit 1.
REPORT NUMBER 50-280/97-001-01 This report has been reviewed by the Station Nuclear Safety and Operating Committee and will be forwarded to the Management Safety Review Committee for its review.
l *,~
~ i n Manager A Christian .
Enclosure Commitments contained in this letter: None.
pc: US Nuclear Regulatory Commission Regional Administrator, Region II Atlanta Federal Center 61 Forsyth Street, SW, Suite 23T85 Atlanta, Georgia 30303 R. A. Musser NRC Senior Resident Inspector Surry Power Station 9706180217 970610 , __
PDR ADOCK 05000280 S PDR Illllll fllll flll(IIIIJJilli! JJII I/JJ /IIJ C 6
- NRG FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY 0MB NO. 3150-0104 (4-95) EXPIRES 4/30/98 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS MANDATORY INFORMATION COLLECTION REQUEST: 50.0 HRS.
REPORTED LESSONS LEARNED ARE INCORPORATED INTO THE LICENSEE EVENT REPORT (LER) LICENSING PROCESS AND FED BACK TO INDUSTRY. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH (T-6 F33),
U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC (See reverse for required number of digits/characters for each block) 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104). OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON. DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) PAGE (3)
SURRY POWER STATION, Unit 1 05000 - 280 1 OF5 TITLE (4)
Shutdown Due to Steam Drain Line Weld Leak EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED 8)
SEQUENTIAL REVISION FACILITY NAME DOCUMENT NUMBER MONTH DAY YEAR YEAR MONTH DAY YEAR NUMBER NUMBER 05000-FACILITY NAME DOCUMENT NUMBER 01 23 97 97 -- 001 -- 01 06 10 91 05000-OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check one or more) (11)
MODE (9) n 20.2201 (b) 20.2203(a)(2}(v) x 50.73(a)(2}(i) 50.73(a)(2)(viii)
POWER 20.2203(a)(1) 20.2203(a)(3}(i) 50.73(a)(2)(ii) 50.73(a)(2}(x)
LEVEL (10) 100 % 20.2203(a)(2}(i) 20.2203(a)(3)(ii) 50.73(a)(2}(iii) 73.71 20.2203(a)(2}(ii} 20.2203(a)(4) 50.73(a)(2)(iv) OTHER 20.2203(a)(2)(iii) 50.36(c}(1) 50.73(a)(2}(v) Specify in Abstract below 20.2203(a)(2)(iv) 50.36(c)(2) 50.73(a)(2}(vii) or in NRG Form 366A LICENSEE CONTACT FOR THIS LER (12 NAME TELEPHONE NUMBER (Include Area Code)
D. A. Christian, Station Manager 1(757) 365-2000 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TO NPRDS TONPRDS X IG DET x999 y SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED MONTH DAY YEAR YES . I X I NO SUBMISSION I (If yes, complete EXPECTED SUBMISSION DATE).
DATE ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced tyoewritten lines) (16)
At 1850 hours0.0214 days <br />0.514 hours <br />0.00306 weeks <br />7.03925e-4 months <br /> on January 23, 1997, with Unit r*and Unit 2 both at 100% power, a 'Service Building Operator performing routine activities in the Unit 1 Main Steam Valve House discovered a small steam leak in the steam drain piping on the " B" main steam line. Unit 1 was shutdown in accordance with the. requirements of Technical Specification 4.15.C.1. While performing normal shutdown procedures, both source range nuclear instruments failed to indicate source range counts, and operator action to manually trip the turbine from the main control room failed to result in a turbine trip.
The turbine was tripped locally at the governor pedestal using the manual trip lever. While shutdown, both source range detectors were replaced, tested and the nuclear instruments were returned to service. The turbine trip actuation circuitry was inspected and tested satisfactorily. The leak was repaired, inspected, and tested prior to returning the Unit to power operation. The health and safety of the public were not affected by this event. A radiological release did not occur. This event was caused by a pin hole leak in a 1 1/2 inch diameter weld. This report is being made pursuant to 10CFR50. 73(a)(2)(i)(A), for any nuclear plant shutdown required by the plant's Technical Soecifications.
NRG FORM 366 (4-95)
i NRG FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (4-95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1) DOCKET LEA NUMBER (6) PAGE (3)
YEAR I SEQUENTIAL NUMBER
- I REVISION NUMBER Surry Unit 1 05000-280 97 --001 -- 01 2 OF 5 TEXT (If more space is required, use additional copies of NRG Form 366A) (17)
1.0 DESCRIPTION
OF THE EVENT Surry Technical Specification 4.15 contains an Augmented Inspection Program requirement that all welds in the Main Steam Valve House receive a visual inspection of the surface of the insulation at all weld locations on a weekly basis for detection of leaks. Any detected leaks shall be investigated and evaluated. If the leakage is caused by a through-wall flaw, either the* plant shall be shutdown, or the leaking piping isolated. Repairs shall be performed prior to return of the line to service.
At approximately 1850 hours0.0214 days <br />0.514 hours <br />0.00306 weeks <br />7.03925e-4 months <br /> on January 23, 1997, a Service Building Operator performing routine duties in the Unit 1 Main Steam Valve House heard a small leak in the vicinity of the steam drain piping on the "B" main steam [EIIS:SB] line. Following further investigation, the Service Building Operator notified the Unit 1 Control Room Operator who informed the Senior Reactor Operator of a steam leak. Maintenance and engineering personnel were assigned to remove the piping insulation and investigate the leak. The insulation was removed by 2225 hours0.0258 days <br />0.618 hours <br />0.00368 weeks <br />8.466125e-4 months <br /> on January 23, 1997 and Engineering personnel identified a pin hole leak approximately 1/32 inch in diameter through a weld in main steam drain line, 1 1/2-SHPD-8-601. Since the steam leak was caused by a through-wall flaw in a weld location that was unisolable, Technical Specification 4.15.C.1 required the plant to be shutdown and repairs performed prior to returning the line to service. At 0124 hours0.00144 days <br />0.0344 hours <br />2.050265e-4 weeks <br />4.7182e-5 months <br /> on January 24, 1997, a Unit 1 shutdown was commenced. At 0143 hours0.00166 days <br />0.0397 hours <br />2.364418e-4 weeks <br />5.44115e-5 months <br /> on January 24, 1997, a one-hour report was made to the NRG in accordance with 10 CFR 50.72(b)(1 )(i)(A) for initiation of any plant shutdown required by Technical Specifications. The Unit was shutdown by 0817 hours0.00946 days <br />0.227 hours <br />0.00135 weeks <br />3.108685e-4 months <br /> on January 24, 1997. A flaw characterization and weld repair were initiated. The failure mechanism was slag entrapment ranging in size from 1/32 to 3/16 inches, located in the weldment.
The flaw was removed by grinding and the weld was repaired. A visual inspection and pressure test were performed and the line was returned to service. This event is reportable in accordance with 10 CFR 50. 73(a)(2)(i)(A) for any plant shutdown required by Technical Specifications.
While ramping the Unit off-line in accordance with normal shutdown procedures the following equipment failures occurred. At .0718 hours0.00831 days <br />0.199 hours <br />0.00119 weeks <br />2.73199e-4 months <br /> on January 24, 1997, when reactor power had been decreased and stabilized at 2 percent, efforts to manually trip the turbine [EIIS:TA] from the Main Control Room using the turbine trip push-buttons [EIIS:IT] in accordance with normal shutdown procedures were unsuccessful. The turbine was tripped locally, at the turbine, using the manual trip lever at 0721 hours0.00834 days <br />0.2 hours <br />0.00119 weeks <br />2.743405e-4 months <br />, and the main generator [EIIS:TB] output breakers were opened. Also, once reactor power was below the point of adding heat and the reactor was tripped in accordance with normal shutdown procedures with the control rods fully inserted and reactor trip breakers open, both source range nuclear instruments [EIIS:IG,JI] energized as expected and then failed to indicate source range counts.
NRC FORM 366A (4-95)
i NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (4-95)
LICENSEE EVENT REPORT {LER)
TEXT CONTINUATION FACILITY NAME (1) DOCKET LER NUMBER (6) PAGE (3)
YEAR I SEQUENTIAL NUMBER I REVISION NUMBER Surry Unit 1 05000-280 97 --001 -- 01 3 OF 5 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
At 0745 hours0.00862 days <br />0.207 hours <br />0.00123 weeks <br />2.834725e-4 months <br /> with both source range nuclear instruments declared inoperable, Abnormal Procedure, 0-AP-4.00, was implemented. The plant was stabilized in the hot shutdown condition with the control rods fully inserted, the reactor trip breakers open, and adequate shutdown margin verified consistent with Action 5 of Technical Specification Table 3.7-1, Item 4.b.
2.0 SIGNIFICANT SAFETY CONSEQUENCES AND IMPLICATIONS There are no safety consequences or implications associated with this event. Flaw characterization and examinations by materials engineering personnel determined the pin hole leak in the weld was an isolated occurrence caused by slag inclusion during original construction which allowed the flaw to slowly propagate to the weld surface after 25 years of service.
The failure of the turbine to trip manually using the Main Control Room push-buttons was a previously analyzed event for which procedures and training were in place to locally trip the turbine using the manual trip lever. Normal shutdown procedures require that reactor power be reduced to less than 2 percent and stabilized prior to tripping the turbine. These procedures allow use of either the Main Control Room push-buttons or the local trip lever to execute a turbine trip and were properly executed during the event. There is no safety significance related to this portion of the event since reactor power had been reduced to 2 percent and stabilized prior to tripping the turbine.
Both source range nuclear instruments energized as required during the shutdown evolution, indicated source range counts, and then fail$-d to properly indicate source range counts after less than 1O minutes of operation. Failure of the source range nuclear instruments had been*
previously evaluated. Procedures and training were in place should such an event occur.
Normal shutdown procedures require that reactor power be reduced below the point of adding heat and stabilized before tripping the reactor and energizing the source range detectors. Upon discovery that the source range nuclear instruments failed, appropriate procedures were properly executed ensuring the plant remained stable in the safe shutdown condition, with all controls rods fully inserted, reactor trip breakers open, and adequate shutdown margin in place in accordance with Action 5 of Technical Specification Table 3.7-1, Item 4.b.
At no time were the health and safety of the public or plant personnel affected by this event.
3.0 CAUSE OF THE EVENT Flaw characterization and examinations by materials engineering personnel determined that the pin hole leak in the weld was an isolated occurrence caused by slag inclusion during original construction which allowed a small flaw to slowly propagate to the weld surface after 25 years of service.-
NRC FORM 366A (4-95)
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (4-95)
LICENSEE EVENT REPORT (LE~
TEXT CONTINUATION FACILITY NAME (1) DOCKET LEA NUMBER (6) PAGE (3)
YEAR I SEQUENTIAL NUMBER l REVISION NUMBER Surry Unit 1 05000 -280 97 --001 -- 01 4 OF 5 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
The unexpected failure of the turbine to trip manually using the Main Control Room push-buttons
- was initially believed to be due to a sluggish auto stop drain valve. Subsequently it was determined to be due to binding within the turbine protective trip block assembly attributable to the lack of turbine protective trip block testing.
The unexpected failure of the source range detectors was initially believed to have been caused by aging. Subsequently this cause was confirmed.
4.0 IMMEDIATE CORRECTIVE ACTION Upon discovery of the steam leak in the Main Steam Valve House the Service Building Operator immediately notified the Unit 1 Control Room Operator. The Unit 1 Senior Reactor Operator notified maintenance personnel and engineering personnel to investigate the leak, and management was notified. Following removal of the piping insulation by maintenance personnel, engineering personnel investigated the leak source and identified the leak to be a pin hole through the wall of a weld in a 1 1/2 inch drain line that could not be isolated. Management was notified and the Shift Supervisor invoked the requirements of Technical Specification 4.15.C.1 and a Unit shutdown commenced.
Upon failure of the turbine to trip when the manual turbine trip push-buttons in the Main Control Room were depressed, the local turbine trip lever on the governor end pedestal was used to trip the turbine. The normal procedure for "Turbine - Generator Shutdown" allows use of either trip mechanism to execute a turbine trip. Following execution of the turbine trip using the turbine trip lever, the main steam stop valves, control valves, reheat stop valves and intercept valves were verified closed; the auto stop oil header was verified to be depressurized; the extraction steam non-return valves were verified shut; and turbine shaft speed was verified to be decreasing.
Upon failure of the source range nuclear instruments to continue, indicating source range counts, Abnormal Procedure, O-AP-4.00, was initiated and the plant was stabilized in the safe shutdown condition. All control rods were verified to be fully inserted, the dilute function to the blender was l maintained under administrative control when not secured, the control rod drive motor /
generator supply breakers were racked to the out position preventing any possible control rod movement, adequate shutdown margin was verified, and positive reactivity additions were prohibited. The gammametric nuclear instruments were verified operable and used as an alternate indication of source range counts. The requirements of Technical Specifications Table
- 3. 7-1 , Item 4, Action 5 were initiated and management was notified.
5.0 ADDITIONAL CORRECTIVE ACTIONS The flaw in the weld was excavated by grinding out the entire portion of the weld encompassing the flaw and performing a weld repair. A visual examination and pressure test were performed to ensure a quality repair was made.
- The insulation was removed from similar welds on the remaining Unit 1 steam drain lines and a visual inspection was performed with no indication of NRC FORM 366A (4-95)
Ii NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION
\ (4-95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1) DOCKET LEA NUMBER (6) PAGE (3)
YEAR I SEQUENTIAL NUMBER l REVISION NUMBER Surry Unit 1 05000-280 97 --001 -- 01 5 OF 5 TEXT (If more space is required, use additional copies of NRC Form 366A) (17) leakage or welding flaws. The piping in the Unit 2 Main Steam Valve House was walked down in accordance with surveillance procedures to ensure a similar leak did not exist.
The turbine trip circuits were tested and verified operational. The turbine control block latch mechanism and suspected sluggish drain valve were inspected and tested to ensure proper operation. A turbine trip functional test was performed to verify proper operation of the manual turbine trip push-buttons and the turbine trip circuit.
The source range nuclear instrument vendor was contacted and a representative was brought on site to assist in the troubleshooting and repair. The source range nuclear instrument, N-32, detector was replaced, tested and returned to service on January 31, 1997. The source range nuclear instrument, N-31, detector was replaced, tested and returned to service on February 1, 1997.
6.0 ACTIONS TO PREVENT RECURRENCE Related to the weld leak, the Augmented Inspection Program requirements will be conducted in accordance with Technical Specification 4.15.
A Root Cause Evaluation, as well as a component functional failure evaluation, required by our Maintenance Rule Program in accordance with 10 CFR 50.65, was performed to investigate the failure of the turbine to trip manually using the Main Control Room push-buttons. This failure was determined to be a Maintenance Rule Functional Failure due to binding within the turbine protective trip block assembly attributable to the lack of turbine protective trip block testing.
Approved recommendations from Root Cause Evaluations are implemented in accordance with the Corrective Action Program.
To investigate the source range nuclear instrument failures, a Root Cause Evaluation was performed with a multidisciplined root cause evaluation team consisting of craft, technical, and engineering personnel assigned to investigate the root cause and recommend corrective actions.
The Root Cause Evaluation, as well as a Maintenance Rule component functional failure evaluation, has been completed. These failures were determined to be a Maintenance Preventable Functional Failure due to component aging. Approved recommendations from Root Cause Evaluations are implemented in accordance with the Corrective Action Program.
7.0 SIMILAR EVENTS There were no similar events identified.
8.0 ADDITIONAL INFORMATION The Source Range Nuclear Instrument detectors are Westinghouse part number WL-24158, serial number 912101.
NRG FORM 366A (4-95)