LER 98-S01-00:on 981105,noted Failure to Deactivate Station Access Badge.Caused by Human Error.Licensee Will Now Deactivate Station Badges Before Clearance Is Revoked & Process for Badge Deactivations Have Been StrengthenedML18152B712 |
Person / Time |
---|
Site: |
Surry  |
---|
Issue date: |
12/04/1998 |
---|
From: |
Grecheck E VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.) |
---|
To: |
|
---|
Shared Package |
---|
ML18152B711 |
List: |
---|
References |
---|
LER-98-S01, LER-98-S1, NUDOCS 9812100128 |
Download: ML18152B712 (4) |
|
Similar Documents at Surry |
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000281/LER-1999-004-02, :on 981109,EDG Was Inoperable Longer than Allowed by TS Due to Governor Compensation Valve.Root Cause Evaluation Being Performed to Determine How Compensation Valve Became Closed1999-10-0101 October 1999
- on 981109,EDG Was Inoperable Longer than Allowed by TS Due to Governor Compensation Valve.Root Cause Evaluation Being Performed to Determine How Compensation Valve Became Closed
05000280/LER-1999-006, :on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With1999-08-27027 August 1999
- on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With
05000280/LER-1999-005-01, :on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed1999-08-27027 August 1999
- on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed
05000280/LER-1999-004-01, :on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms1999-08-13013 August 1999
- on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms
05000281/LER-1999-003-02, :on 990705,auto Reactor Trip on Low Coolant Flow,Occurred.Caused by Loop Stop Valve Failure.Approved RCE Recommendations,Designed to Prevent Recurrence of Similar Event Will Be Implemented Through CAP1999-07-30030 July 1999
- on 990705,auto Reactor Trip on Low Coolant Flow,Occurred.Caused by Loop Stop Valve Failure.Approved RCE Recommendations,Designed to Prevent Recurrence of Similar Event Will Be Implemented Through CAP
05000281/LER-1999-002-02, :on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With1999-05-18018 May 1999
- on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With
05000280/LER-1999-003-01, :on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With1999-04-28028 April 1999
- on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With
05000281/LER-1999-001-02, :on 990301,RPS Relay Not Placed in Trip Resulted in Violation of TS 3.7.Caused by Lack of Procedural Guidance.Developed New Procedure to Provide More Explicit Instructions for Placing Stop Valve in Relay Trip1999-03-31031 March 1999
- on 990301,RPS Relay Not Placed in Trip Resulted in Violation of TS 3.7.Caused by Lack of Procedural Guidance.Developed New Procedure to Provide More Explicit Instructions for Placing Stop Valve in Relay Trip
05000280/LER-1999-002-01, :on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 9902121999-03-29029 March 1999
- on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212
05000280/LER-1998-013, :on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr1999-03-19019 March 1999
- on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr
05000280/LER-1999-001, :on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable1999-01-21021 January 1999
- on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable
05000280/LER-1998-014, :on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition1998-12-16016 December 1998
- on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition
ML18152B7121998-12-0404 December 1998 LER 98-S01-00:on 981105,noted Failure to Deactivate Station Access Badge.Caused by Human Error.Licensee Will Now Deactivate Station Badges Before Clearance Is Revoked & Process for Badge Deactivations Have Been Strengthened 05000280/LER-1998-012, :on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With1998-12-0101 December 1998
- on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With
05000280/LER-1998-010, :on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status1998-07-31031 July 1998
- on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status
05000280/LER-1998-009, :on 980509,nonisolable Leak of Reactor Coolant Pump Seal Injection Line Weld,Was Discovered.Caused by Lack of Fusion or Thermal Fatigue Coupled W/Vibration Stress Due to Loose Rod Hanger.Rcp Seal Injection Line Removed1998-06-0303 June 1998
- on 980509,nonisolable Leak of Reactor Coolant Pump Seal Injection Line Weld,Was Discovered.Caused by Lack of Fusion or Thermal Fatigue Coupled W/Vibration Stress Due to Loose Rod Hanger.Rcp Seal Injection Line Removed
05000280/LER-1998-008, :on 980228,auxiliary Ventilation Fans Were Noted in Condition Outside of Design Basis.Caused by Failure to Recognize Potential Impact of Certain Design Basis Accident Scenarios.No Corrective Actions Needed1998-05-22022 May 1998
- on 980228,auxiliary Ventilation Fans Were Noted in Condition Outside of Design Basis.Caused by Failure to Recognize Potential Impact of Certain Design Basis Accident Scenarios.No Corrective Actions Needed
05000280/LER-1998-007, :on 980330,radiation Monitors Were Declared Inoperable.Caused by Change in Operating Temperature Range. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-61998-04-29029 April 1998
- on 980330,radiation Monitors Were Declared Inoperable.Caused by Change in Operating Temperature Range. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-6
05000280/LER-1998-006, :on 980324,unisolable Through Wall Leak of RCP Thermowell Was Noted.Cause of Leak Is Unknown.Rtd Will Be Replaced1998-04-22022 April 1998
- on 980324,unisolable Through Wall Leak of RCP Thermowell Was Noted.Cause of Leak Is Unknown.Rtd Will Be Replaced
05000280/LER-1998-005, :on 980212,fire Watch Insp Exceeded One Hour. Caused by Lack of Attention to Detail by Individual Involved.Individual Involved Was Coached on Requirement to Perform Fire Watch Patrols within Required Time Frame1998-04-22022 April 1998
- on 980212,fire Watch Insp Exceeded One Hour. Caused by Lack of Attention to Detail by Individual Involved.Individual Involved Was Coached on Requirement to Perform Fire Watch Patrols within Required Time Frame
05000280/LER-1998-003, :on 980226,no Procedural Guidance for Maintaining EDG Minimum Fuel Supply During Loop,Was Identified.Caused by Absence of Procedural Instructions. Deviation Rept Submitted to Document Deviating Condition1998-03-0909 March 1998
- on 980226,no Procedural Guidance for Maintaining EDG Minimum Fuel Supply During Loop,Was Identified.Caused by Absence of Procedural Instructions. Deviation Rept Submitted to Document Deviating Condition
05000280/LER-1998-004, :on 980206,fire Watch Was Released Prematurely Resulting in Violation of Ts.Caused by Inadequate Planning of Repair Activity.Work Orders Will Include Ref to Applicable Procedures Developed to Assist in Repairs1998-03-0606 March 1998
- on 980206,fire Watch Was Released Prematurely Resulting in Violation of Ts.Caused by Inadequate Planning of Repair Activity.Work Orders Will Include Ref to Applicable Procedures Developed to Assist in Repairs
05000280/LER-1998-002, :on 980202,automatic Turbine Trip Resulted in Automatic Reactor Trip.Caused Degraded Generator Voltage Regulator sub-component Failure.Placed Plant in Safe Hot SD & Replaced Intermittent Relay & Relay Socket1998-03-0404 March 1998
- on 980202,automatic Turbine Trip Resulted in Automatic Reactor Trip.Caused Degraded Generator Voltage Regulator sub-component Failure.Placed Plant in Safe Hot SD & Replaced Intermittent Relay & Relay Socket
05000280/LER-1998-001-01, :on 980108,deficient Test Due to Faulty Test Equipment Resulted in TS Violation.Caused by Faulty Vibration Analyzer Cable or Loose Connection.Station Deviation Rept Was Submitted1998-02-0606 February 1998
- on 980108,deficient Test Due to Faulty Test Equipment Resulted in TS Violation.Caused by Faulty Vibration Analyzer Cable or Loose Connection.Station Deviation Rept Was Submitted
05000280/LER-1997-009, :on 971014,declared Intake Canal Level Probes Inoperable Due to Marine Growth.Caused by Inadequate Maint of Intake Canal Level Probes.Subject Probes Were Cleaned, Tested Satisfactorily & Returned to Operable Status1998-01-13013 January 1998
- on 971014,declared Intake Canal Level Probes Inoperable Due to Marine Growth.Caused by Inadequate Maint of Intake Canal Level Probes.Subject Probes Were Cleaned, Tested Satisfactorily & Returned to Operable Status
05000280/LER-1997-012, :on 971028,loss of Power to Latching Mechanism on Several Doors Occurred.Caused by Tripping of Two Breakers in Security Distribution Panel.Reset Affected Breakers Which Restored Power to Security Systems & Affected Doors1998-01-13013 January 1998
- on 971028,loss of Power to Latching Mechanism on Several Doors Occurred.Caused by Tripping of Two Breakers in Security Distribution Panel.Reset Affected Breakers Which Restored Power to Security Systems & Affected Doors
05000281/LER-1997-004-02, :on 971202,invalid Mstv Indication Results in Manual Reactor Trip W/Esf Actuation Were Noted.Caused by Displaced Open Limit Switch Arms.Open Limit Switch for Mstv a Was Relocated Closer to Valve Position Bar1997-12-31031 December 1997
- on 971202,invalid Mstv Indication Results in Manual Reactor Trip W/Esf Actuation Were Noted.Caused by Displaced Open Limit Switch Arms.Open Limit Switch for Mstv a Was Relocated Closer to Valve Position Bar
05000281/LER-1997-002-01, :on 970713,main Steam High Range Radiation Monitor Was Declared Inoperable.Caused by Equipment Failure. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-61997-12-10010 December 1997
- on 970713,main Steam High Range Radiation Monitor Was Declared Inoperable.Caused by Equipment Failure. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-6
05000280/LER-1997-011, :on 971030,determined That Periodic Test Procedures for Testing Reactor Trip Bypass Breakers Did Not Test Manual Undervoltage Trip.Caused by mis-interpretation of Term in-service. Procedures Revised1997-11-26026 November 1997
- on 971030,determined That Periodic Test Procedures for Testing Reactor Trip Bypass Breakers Did Not Test Manual Undervoltage Trip.Caused by mis-interpretation of Term in-service. Procedures Revised
05000280/LER-1997-010, :on 971028,discovered Missed Fire Protection Surveillance Pt.Caused by Personnel Error.Satisfactorily Completed PT Procedure 0-OPT-FP-009 & Diesel Driven Fire Pump 1-FP-P-2 Declared Operable1997-11-25025 November 1997
- on 971028,discovered Missed Fire Protection Surveillance Pt.Caused by Personnel Error.Satisfactorily Completed PT Procedure 0-OPT-FP-009 & Diesel Driven Fire Pump 1-FP-P-2 Declared Operable
05000281/LER-1997-003-02, :on 971014,Unit 2 MSSVs Revealed That Lift Setting for Two MSSVs Were Outside as Found Setpoint Tolerance.Caused by Minor Setpoint Drift.Repaired,Revised & Adjusted Safety Valves1997-11-13013 November 1997
- on 971014,Unit 2 MSSVs Revealed That Lift Setting for Two MSSVs Were Outside as Found Setpoint Tolerance.Caused by Minor Setpoint Drift.Repaired,Revised & Adjusted Safety Valves
05000280/LER-1997-008-01, :on 971011,invalid Actuation of ESF Occurred. Caused by Personnel Errors.Main CR Bottled Air Sys Isolated & Containment Hydrogen Analyzer Heat Tracing Actuation Signal Reset1997-11-0707 November 1997
- on 971011,invalid Actuation of ESF Occurred. Caused by Personnel Errors.Main CR Bottled Air Sys Isolated & Containment Hydrogen Analyzer Heat Tracing Actuation Signal Reset
05000280/LER-1997-007-01, :on 970930,determined That Plant Was Outside App R Design Basis Due to Vital Bus Isolation Issue.Caused by Personnel Error.Installed Circuit Protective Device During Oct 1997 Refueling Outage1997-10-30030 October 1997
- on 970930,determined That Plant Was Outside App R Design Basis Due to Vital Bus Isolation Issue.Caused by Personnel Error.Installed Circuit Protective Device During Oct 1997 Refueling Outage
05000281/LER-1997-002-03, :on 970713,CR annunciator,2-RMA-A-7 for Main Steam Line Effluent High Range Radiation Monitors Alarmed. Caused by Intermittent Component Failure.Preplanned Alternate Method of Monitoring Initiated1997-08-12012 August 1997
- on 970713,CR annunciator,2-RMA-A-7 for Main Steam Line Effluent High Range Radiation Monitors Alarmed. Caused by Intermittent Component Failure.Preplanned Alternate Method of Monitoring Initiated
05000280/LER-1997-001, :on 970123,shutdown Occurred Due to Drain Line Weld Leak.Inspected & Tested Turbine Trip Actuation Circuitry1997-06-10010 June 1997
- on 970123,shutdown Occurred Due to Drain Line Weld Leak.Inspected & Tested Turbine Trip Actuation Circuitry
05000280/LER-1997-005, :on 970502,Unit 1 Power Range Nuclear Instrumentation Was Inoperable Due to Personnel Error.Sro & STA That Were Involved in Event Were Counseled1997-05-28028 May 1997
- on 970502,Unit 1 Power Range Nuclear Instrumentation Was Inoperable Due to Personnel Error.Sro & STA That Were Involved in Event Were Counseled
05000280/LER-1997-006, :on 970320,loss of Refueling Integrity Due to Inadequate Containment Closure Process & Verification.Fuel Movement Stopped IAW Action Statement Requirements of TS 3.10.B1997-04-18018 April 1997
- on 970320,loss of Refueling Integrity Due to Inadequate Containment Closure Process & Verification.Fuel Movement Stopped IAW Action Statement Requirements of TS 3.10.B
05000280/LER-1997-004, :on 970317,main Steam Safety Valve Was Outside as Found Setpoint Tolerance.Specific Cause Unknown,However, Minor Setpoint Drift Can Be Expected.No Immediate Corrective Actions Performed1997-04-15015 April 1997
- on 970317,main Steam Safety Valve Was Outside as Found Setpoint Tolerance.Specific Cause Unknown,However, Minor Setpoint Drift Can Be Expected.No Immediate Corrective Actions Performed
05000280/LER-1997-002, :on 970116,one Train of Auxiliary Ventilation Sys Was Inoperable Outside of Ts.Caused by Personnel Error. Submitted Deviation Rept Re Reverse Rotation of Fan & Work Request to Adjust Linkage1997-04-0808 April 1997
- on 970116,one Train of Auxiliary Ventilation Sys Was Inoperable Outside of Ts.Caused by Personnel Error. Submitted Deviation Rept Re Reverse Rotation of Fan & Work Request to Adjust Linkage
05000281/LER-1997-001-01, :on 970218,manual Reactor Trip & ESF Actuation Occurred Due to Loss of EHC Control Power.Caused by Momentary Short.Relay Card Was Replaced1997-03-19019 March 1997
- on 970218,manual Reactor Trip & ESF Actuation Occurred Due to Loss of EHC Control Power.Caused by Momentary Short.Relay Card Was Replaced
05000280/LER-1997-003, :on 970219,loss of Pressurizer Heaters Resulted in Manual U1 Trip & U2 ESF Actuation.Caused by Loss of Group C Pressurizer Proportional Heaters.Reactor Trip Breakers Were Verified Open1997-03-19019 March 1997
- on 970219,loss of Pressurizer Heaters Resulted in Manual U1 Trip & U2 ESF Actuation.Caused by Loss of Group C Pressurizer Proportional Heaters.Reactor Trip Breakers Were Verified Open
05000280/LER-1997-002-01, :on 970116,one Train of Auxiliary Ventilation Sys Declared Inoperable.Caused by Personnel Error.Properly Adjusted Damper 1-VS-MOD-58B & Exited Seven Day LCO on 9701161997-02-13013 February 1997
- on 970116,one Train of Auxiliary Ventilation Sys Declared Inoperable.Caused by Personnel Error.Properly Adjusted Damper 1-VS-MOD-58B & Exited Seven Day LCO on 970116
05000281/LER-1997-002, :on 961213,automatic Reactor Trip Occurred During Planned Shutdown.Caused by Steam Flow/Feedwater Flow Mismatch.Rps Functioned as Designed & Plant Placed in Hot Shutdown1997-01-0202 January 1997
- on 961213,automatic Reactor Trip Occurred During Planned Shutdown.Caused by Steam Flow/Feedwater Flow Mismatch.Rps Functioned as Designed & Plant Placed in Hot Shutdown
05000280/LER-1996-008-01, :on 961112,water Gas Decay Tank Oxygen Analyzer Pressure Sensors Inoperable Due to Vendor Supplied Equipment Not Meeting Procurement specifications.Post-implementation Procedures Revised & Transducers Replaced1996-12-12012 December 1996
- on 961112,water Gas Decay Tank Oxygen Analyzer Pressure Sensors Inoperable Due to Vendor Supplied Equipment Not Meeting Procurement specifications.Post-implementation Procedures Revised & Transducers Replaced
05000280/LER-1996-007, :on 960821,failed to Complete Fire Detection Zone Inspections within Required Time Period.Caused by Personnel Error.Counseled Personnel Re Fire Detection Zone Inspections & Revised Fire Watch Training1996-09-19019 September 1996
- on 960821,failed to Complete Fire Detection Zone Inspections within Required Time Period.Caused by Personnel Error.Counseled Personnel Re Fire Detection Zone Inspections & Revised Fire Watch Training
05000281/LER-1996-005-01, :on 960803,manual Reactor Trip.Caused by Loss of Electro Hydraulic Control Pressure.Repaired Two Compression Fitting Union Connections on Leaking Fitting & Performed Evaluations on Other Tubing1996-08-26026 August 1996
- on 960803,manual Reactor Trip.Caused by Loss of Electro Hydraulic Control Pressure.Repaired Two Compression Fitting Union Connections on Leaking Fitting & Performed Evaluations on Other Tubing
05000280/LER-1996-006, :on 960618,anti-corrosion Coating Had Not Been Reapplied to Station Battery 2B.Caused by Procedural Error in That Verbatim TS Compliance Not Reflected in Procedures. Coating Was Applied to Batteries1996-07-30030 July 1996
- on 960618,anti-corrosion Coating Had Not Been Reapplied to Station Battery 2B.Caused by Procedural Error in That Verbatim TS Compliance Not Reflected in Procedures. Coating Was Applied to Batteries
05000281/LER-1996-004-02, :on 960606,turbine/reactor Trip Occurred.Caused by High Level in Steam Generator B.Placed Plant in Hot Shutdown Condition,Calculated Shutdown Margin & Monitored Critical Safety Function Status Trees1996-07-0202 July 1996
- on 960606,turbine/reactor Trip Occurred.Caused by High Level in Steam Generator B.Placed Plant in Hot Shutdown Condition,Calculated Shutdown Margin & Monitored Critical Safety Function Status Trees
05000280/LER-1996-004, :on 960510,noticed That Hydrogen Analyzers Inoperable.Caused by Procedural Deficiencies Due to Personnel Error.Permanent Changes to Hydrogen Analyzer Instrument Calibr Procedures Implemented1996-06-10010 June 1996
- on 960510,noticed That Hydrogen Analyzers Inoperable.Caused by Procedural Deficiencies Due to Personnel Error.Permanent Changes to Hydrogen Analyzer Instrument Calibr Procedures Implemented
05000281/LER-1996-003-01, :on 960512,Unit 2 Pressurizer Safety Valve as Found Lift Setting Out of Tolerance.Valve Was Reassembled & Lift Setting Was Established & Tested Satisfactorily1996-06-0707 June 1996
- on 960512,Unit 2 Pressurizer Safety Valve as Found Lift Setting Out of Tolerance.Valve Was Reassembled & Lift Setting Was Established & Tested Satisfactorily
1999-08-27
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18152A2811999-10-12012 October 1999 Technical Basis for Elimination of Nozzle Inner Radius Insps (for Nozzles Other than Reactor Vessel),Technical Basis for ASME Section XI Code Case N-619 05000281/LER-1999-004-02, :on 981109,EDG Was Inoperable Longer than Allowed by TS Due to Governor Compensation Valve.Root Cause Evaluation Being Performed to Determine How Compensation Valve Became Closed1999-10-0101 October 1999
- on 981109,EDG Was Inoperable Longer than Allowed by TS Due to Governor Compensation Valve.Root Cause Evaluation Being Performed to Determine How Compensation Valve Became Closed
ML18152B3531999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Surry Power Station,Units 1 & 2.With ML18152B3371999-09-24024 September 1999 SER Accepting Third 10-year Interval Inservice Insp Plan Request for Relief SR-026 for Surry Power Station Unit 2 ML18152B6651999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Surry Power Station Units 1 & 2.With 05000280/LER-1999-006, :on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With1999-08-27027 August 1999
- on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With
05000280/LER-1999-005-01, :on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed1999-08-27027 August 1999
- on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed
ML18152B3841999-08-23023 August 1999 Safety Evaluation Granting Relief Request from ASME Section Xa Requirements for Containment Insp ML18152B3631999-08-23023 August 1999 Safety Evaluation Supporting Eddy Current Techniques Used by VEPCO to Determine Depth of Degradation Evident in Units SG Tubing & VEPCO Approach for Dispositioning Tubes with Avb Wear Indications ML18152B3831999-08-23023 August 1999 Safety Evaluation Granting Relief Request from ASME Section XI Requirements for Containment Insp 05000280/LER-1999-004-01, :on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms1999-08-13013 August 1999
- on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms
ML18151A3981999-08-13013 August 1999 SPS Unit 2 ISI Summary Rept for 1999 Refueling Outage ML18152B3791999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Surry Power Station,Units 1 & 2.With 05000281/LER-1999-003-02, :on 990705,auto Reactor Trip on Low Coolant Flow,Occurred.Caused by Loop Stop Valve Failure.Approved RCE Recommendations,Designed to Prevent Recurrence of Similar Event Will Be Implemented Through CAP1999-07-30030 July 1999
- on 990705,auto Reactor Trip on Low Coolant Flow,Occurred.Caused by Loop Stop Valve Failure.Approved RCE Recommendations,Designed to Prevent Recurrence of Similar Event Will Be Implemented Through CAP
ML20196J4781999-07-0101 July 1999 Safety Evaluation Supporting Amends 221 & 221 to Licenses DPR-32 & DPR-37,respectively ML18152B3911999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Surry Power Station,Units 1 & 2.With ML20195D3571999-06-0707 June 1999 Safety Evaluation Supporting Amends 220 & 220 to Licenses DPR-32 & DPR-37,respectively ML20195E2401999-05-31031 May 1999 Rev 2 to COLR for SPS Unit 2 Cycle 16 Pattern Ag ML18152B4341999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Surry Power Station,Units 1 & 2.With 05000281/LER-1999-002-02, :on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With1999-05-18018 May 1999
- on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With
ML18152B4161999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Surry Power Station Units 1 & 2.With 05000280/LER-1999-003-01, :on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With1999-04-28028 April 1999
- on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With
ML18152B6481999-04-14014 April 1999 Safety Evaluation Supporting Relief Requests IWE-2,4.5.6 & IWL-2 to Licenses DPR-32 & DPR-37 Respectively ML18152B6451999-04-13013 April 1999 SER Accepting Util Reactor Pressure Vessel Fluence Methodology for Surry Power Stations,Units 1 & 2 & North Anna Power Station,Units 1 & 2 Subject to Listed Limitations 05000281/LER-1999-001-02, :on 990301,RPS Relay Not Placed in Trip Resulted in Violation of TS 3.7.Caused by Lack of Procedural Guidance.Developed New Procedure to Provide More Explicit Instructions for Placing Stop Valve in Relay Trip1999-03-31031 March 1999
- on 990301,RPS Relay Not Placed in Trip Resulted in Violation of TS 3.7.Caused by Lack of Procedural Guidance.Developed New Procedure to Provide More Explicit Instructions for Placing Stop Valve in Relay Trip
ML18152B6511999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Surry Power Station Units 1 & 2 05000280/LER-1999-002-01, :on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 9902121999-03-29029 March 1999
- on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212
05000280/LER-1998-013, :on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr1999-03-19019 March 1999
- on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr
ML20207L8081999-03-12012 March 1999 Safety Evaluation Supporting Amends 219 & 219 to Licenses DPR-32 & DPR-37 ML18152B7331999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Surry Power Station,Units 1 & 2.With ML18152B5381999-02-16016 February 1999 SER Accepting Third 10-year Interval Inservice Insp Request for Relief for Surry Power Station,Unit 1.Staff Concludes That Licensee Proposed Alternative Will Provide Acceptable Level of Quality & Safety.Technical Ltr Rept Also Encl ML18152B5421999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Surry Power Station,Units 1 & 2.With ML18151A3031999-01-29029 January 1999 ISI Summary Rept for 1998 Refueling Outage,Including Form NIS-1, Owners Rept for ISIs & Form NIS-2, Owners Rept for Repairs & Replacements 05000280/LER-1999-001, :on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable1999-01-21021 January 1999
- on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable
ML18152B6011998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Surry Power Station,Units 1 & 2.With ML18152B5861998-12-18018 December 1998 SER Approving Request Relief Related to Inservice Testing Program at Surry Power Station Unit 1 ML20198F9221998-12-16016 December 1998 Safety Evaluation Supporting Amends 217 & 217 to Licenses DPR-32 & DPR-37,respectively 05000280/LER-1998-014, :on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition1998-12-16016 December 1998
- on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition
ML18152B5901998-12-16016 December 1998 Safety Evaluation Authorizing Request to Use Code Case N-577 as Alternative to Requirements of ASME Code Section XI for Surry Power Station,Unit 1 ML18152B7121998-12-0404 December 1998 LER 98-S01-00:on 981105,noted Failure to Deactivate Station Access Badge.Caused by Human Error.Licensee Will Now Deactivate Station Badges Before Clearance Is Revoked & Process for Badge Deactivations Have Been Strengthened 05000280/LER-1998-012, :on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With1998-12-0101 December 1998
- on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With
ML18152B7081998-11-30030 November 1998 Rev 0 to COLR for Surry 1 Cycle 16,Pattern Un ML18152B5721998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Surry Power Station,Units 1 & 2.With ML18152B6241998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Surry Power Station Units 1 & 2.With ML18152B6881998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Surry Power Station Units 1 & 2.With ML20151U7261998-09-0303 September 1998 Safety Evaluation Approving Exemption from Certain 10CFR20 Requirements Re Use of self-contained Breathing Apparatus with Enriched Oxygen in Subatmospheric Containments at SPS ML18153A3271998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Surry Power Station,Units 1 & 2 ML20237E9721998-08-26026 August 1998 Safety Evaluation Supporting Amends 216 & 216 to Licenses DPR-32 & DPR-37,respectively ML18153A3161998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Surry Power Station Units 1 & 2 05000280/LER-1998-010, :on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status1998-07-31031 July 1998
- on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status
1999-09-30
[Table view] |
Text
--~-
e e
NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY 0MB NO. 3150-0104 EXPIRES 06/30/2001 (6-1998)
Estimated burden per response to comply with this mand~tory informa!ion collection request: 50 hrs. Reported lessons learned are incorporated rnto LICENSEE EVENT REPORT (LER) the licensing process and fed back to industry. Forward comments regarding burden estimate to the Records Management Branch (T -6 F33),
U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, and to (See reverse for required number of the Paperwork Reduction Project (3150-0104), Office of Management and Budget, Washington, DC 20503.
If an information collection does not digits/characters for each block) display a currently valid 0MB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
FACILITY NAME (1)
DOCKET NUMBER (2)
PAGE(3)
SURRY POWER STATION, Unit 1 05000- 280 1 OF 4 TITLE (4)
Failure to Terminate Access Results in Unauthorized Protected Area Entry EVENT DATE (5)
LER NUMBER 6)
REPORT DATE m OTHER FACILITIES INVOLVED 8)
FACILITY NAME DOCKET NUMBER I
SEQUENTIAL REVISION Surrv Unit 2 05000 -- 281 MONTH DAY
- YEAR YEAR NUMBER NUMBER MONTH DAY YEAR FACILITY NAME DOCKET NUMBER 11 05 1998 1998 -
S01 00 12 04 1998 n"nnn OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check one or more) (11)
MODE (9)
N 20.2201(b) 20.2203(a)(2)(v)
- 50. 73(a)(2)(i)
- 50. 73{a)(2)(viii) 20.2203(a)(1) 20.2203{a)(3){i)
- 50. 73(a)(2)(ii)
- 50. 73(a)(2)(xl L 10 0%
20.2203{a){2)(i) 20.2203(a)(3Hiil
- 50. 73{a)(2)(iiil X 73.71 20.2203{aH2Hiil 20.2203(a)(4)
- 50. 73(aH2Hiv)
OTHER 20.2203(a)(2)(iii) 50.36(c){1) 50.73(a)(2)(v)
Specify in Abstract below or 20.2203(a)(2){iv) 50.36{c)(2) 50.73(a)(2)(vii) in NRC Form 366A LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER (Include Area Code)
E. S. Grecheck, Site Vice President (757) 365-2000 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
REPORTABLE REPORTABLE CAUSE SYSTEM COMPONENT MANUFACTURER TO EPIX CAUSE SYSTEM COMPONENT MANUFACTURER TO EPIX
::{
'.i.
J}!
SUPPLEMENTAL REPORT EXPECTED (14)
EXPECTED MONTH DAY YEAR IYES Ix !No SUBMISSION (If yes, complete EXPECTED SUBMISSION DATE).
DATE (15)
ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16)
On June 22, 1998, based upon the request of the employee's company, clearance for unescorted access was revoked for a Freeze Seal employee by a Corporate Nuclear Access Specialist. The revocation of the individual's clearance did not result in the deactivation of the individual's station access badge. The failure to deactivate the station access badge was due to a human error. A contributing factor was the design interface between the computer systems that maintain the information on a worker's access authorization and the station access control computer systems. If clearance is revoked, station personnel must manually deactivate the access badge in the access control computers.
On August 11, 1998, at 1149 hours0.0133 days <br />0.319 hours <br />0.0019 weeks <br />4.371945e-4 months <br />, with Units 1 and 2 at 100% power, the Freeze Seal employee entered the protected area (PA) to retrieve company equipment left from a previous job. At 1159 hours0.0134 days <br />0.322 hours <br />0.00192 weeks <br />4.409995e-4 months <br />, the individual exited the PA.
On November 4, 1998, a Freeze Seal representative called to re-establish clearance for the same Freeze Seal employee. A review determined that his badge was still active and the individual entered the PA once after his company requested revocation of clearance in June.
A station deviation report was filed and a 1-hour report was issued in accordance with 1 O CFR 73. 71 (b)(1) due to an actual entry of an unauthorized person into the PA. A root cause evaluation was initiated.
Station badges are now deactivated before clearance is revoked and the processes for badge deactivations have been strenathener:L ThP. report is being submitted as required by 10 CFR 73. 71 (d).
9812100128 981204 PDR ADOCK 05000280 S
PDR
NRC FORM 366A (6-1998) e FACILITY NAME (1)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION D0CKET(2)
SURRY POWER STATION, Unit 1 05000 ** 280 TEXT (If more space is required, use additional copies of NRG Form 366A) (17)
1.0 DESCRIPTION
OF THE EVENT e
U.S. NUCLEAR REGULATORY COMMISSION LER NUMBER 6)
PAGE (3)
I SEQUENTIAL REVISION YEAR NUMBER NUMBER 1998 -
S01 00 2 OF 4 On June 22, 1998, Nuclear Access Services (NAS/Corporate) received a letter from the Vice President Administration, Freeze Seal Incorporated (contractor), indicating that an employee of their company no longer required clearance for Virginia Electric and Power Company (VEPCO) nuclear facilities. A Nuclear Access Specialist processed the favorable termination request by revoking the individual's clearance in the Corporate Security Information System (CSIS) database.
On June 23, 1998, at 0050 hours5.787037e-4 days <br />0.0139 hours <br />8.267196e-5 weeks <br />1.9025e-5 months <br />, a Daily Clearances Processing Report for June 22, 1998, was generated by the CSIS computer and printed at the station. The report listed all the clearance revocations processed on the referenced date, including the Freeze Seal employee.
To complete the normal processing of favorable termination requests, the badging coordinator at the station reviewed the above report on June 23, 1998. Security badges for the individuals listed on the report were deactivated in the station's access control computer systems (Sentracon computer, Hand Geometry Unit system, and Badge Management System). The station badge coordinator, however, failed to deactivate the badge for the Freeze Seal employee. Verification of the badge deactivation process was performed on June 24, 1998, by reviewing a Badge Activation/Deactivation Report generated by the CSIS computer for work completed on June 23, 1998.
The report was compared to individual badge data sheets which maintain a history on each badge. This verification was inadequate because no badge data sheets were pulled and edited for the Freeze Seal employee.
On August 11, 1998, the same Freeze Seal employee was sent to the station to retrieve company equipment left from a previous job. He verified with the badging coordinator that his badge was still active and at 1149 hours0.0133 days <br />0.319 hours <br />0.0019 weeks <br />4.371945e-4 months <br />, with Units 1 and 2 at 100% power, the Freeze Seal employee entered the protected. area (PA). At 1159 hours0.0134 days <br />0.322 hours <br />0.00192 weeks <br />4.409995e-4 months <br />, the same individual exited the PA.
On November 4, 1998, a Freeze Seal representative called NAS to determine the procedure for re-establishing clearance for the Freeze Seal employee for whom Freeze Seal had requested revocation of access authorization on June 22, 1998.
It was discovered during the review for re-instatement, that the CSIS database indicated that the individual's badge was still active. Station security was notified by NAS and the Security Shift Leader verified that the Freeze Seal employee's badge was still active in the station's access control computer systems. The badge was then deactivated on November 4, 1998 at 1700 hours0.0197 days <br />0.472 hours <br />0.00281 weeks <br />6.4685e-4 months <br />.
On November 5, 1998, a search was performed on the access history of the Freeze Seal NRC FORM 366A (6-1998)
=---
!~.-----=--~-
NRC FORM 366A (6-1998)
F'ACILITY NAME (1)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION D0CKET(2)
SURRY POWER STATION, Unit 1 05000 -- 280 TEXT (If more space is required, use additional copies of NRG Form 366A) (17) e U.S. NUCLEAR REGULATORY COMMISSION LEA NUMBER (6)
PAGE (3)
YEAR I SEQUENTIAL I REVISION NUMBER NUMBER 1998 -
S01 00 3 OF 4 employee. The search determined that the individual entered the PA once since June 22, 1998. A deviation report was submitted to document the event. After review of reportability requirements, a 1-hour report was issued at 1831 hours0.0212 days <br />0.509 hours <br />0.00303 weeks <br />6.966955e-4 months <br /> on November 5, 1998, in accordance with 1 O CFR 73.71 (b)(1) due to an actual entry of an unauthorized person into the protected area.
2.0 SIGNIFICANT SAFETY CONSEQUENCES AND IMPLICATIONS The request and subsequent revocation of the Freeze Seal employee's clearance was considered a favorable termination. The duration of entry into the PA was limited to 1 O minutes on August 11, 1998. There was no "intrusion" into the protected area by an unauthorfzed individual. There was no m~levolent attempt to access the protected area.
This event posed no potential to endanger the public health and safety or national security, as indicated by the examples provided in Regulatory Guide 5.62, revision 1.
A review of the Freeze Seal employee's current qualification indicated that after completion of a routine Fitness for Duty screening, full re-instatement of access to the station would have been authorized.
3.0 CAUSE
- The cause of the event was human error.
The station badging coordinator failed to deactivate the individual's badge when the Daily Clearance Processing Report for June 22, 1998 was reviewed and processed at the station on June 23, 1998.
In addition, the process used to verify completeness, accuracy, and error detection for the clearances that were issued or revoked by the Corporate NAS staff was inadequate. The Badge Activation/Deactivation Report generated by the CSIS computer for work completed on June 23, 1998 was compared to the individual badge data sheets, which maintain a history on each badge. Since the Freeze Seal employee's revocation of clearance was missed on June 23, 1998, his badge data sheet was not pulled for review and deactivation of his badge did not appear on the Badge Activation/Deactivation Report generated on June 24, 1998.
Contributing to the event was the design interface between the computer systems that maintain the information on worker's clearance and the station access control computer*
systems. If a clearance is revoked in the CSIS computer, badge deactivation at the station requires manual input for three computer systems.
NRC FORM 366A (6-1998)
NRC FORM 366A (6-1998) e FACILITY NAME (1)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION D0CKET(2)
SURRY POWER STATION, Unit 1 05000 -- 280 TEXT (If more space is required, use additional copies of NRG Form 366A) (17) 4.0 IMMEDIATE CORRECTIVE ACTION(S) e U.S. NUCLEAR REGULATORY COMMISSION LEA NUMBER 6)
PAGE (3)
I SEQUENTIAL REVISION YEAR NUMBER NUMBER 1998 -
S01 - --
00 4 OF 4 The station on-duty security shift was notified by NAS and the Freeze Seal employee's badge was verified to be active. The badge was removed from the station's access control computer systems on November 4, 1998 at 1700 hours0.0197 days <br />0.472 hours <br />0.00281 weeks <br />6.4685e-4 months <br />.
A review was conducted to determine if the individual had entered the protected area with revoked clearance. When the review identified that the individual had entered the PA one time after his clearance was revoked, a station deviation report was submitted on November 5, 1998.
5.0 ADDITIONAL CORRECTIVE ACTIONS A review was conducted to determine if there were other individuals with active badges but without a clearance. The review concluded that this was an isolated event and there were no other individuals with active badges and revoked clearances.
A root cause evaluation (RCE) was initiated.
Before revoking clearance for unescorted access, the NAS staff has been directed to review the CSIS to determine if the individual has an active badge at the station. If the badge is active in the CSIS computer,* NAS will notify the station badge coordinator to deactivate the badge before NAS will revoke the clearance.
To verify completeness and accuracy of badge activation/deactivation, the station badging coordinator and the shift badging personnel have been directed to review the access authorization list generated from the station's access control computer system with the Daily Clearance Processing Report. This will ensure that revoked clearances listed on the Daily Clearance Processing Report do not have active badges in the station's access control computer.
6.0 ACTIONS TO PREVENT RECURRENCE The above corrective actions will strengthen the barriers to prevent a recurrence of this event. Recommendations from the RCE, deemed necessary to _prevent recurrence, will be implemented when the evaluation is complete.
7.0 SIMILAR EVENTS None NRC FORM 366A (6-1998)