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{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION REGION III 2443 WARRENVILLE ROAD, SUITE 210 LISLE, IL 60532-4352  February 7, 2012 Mr. Michael J. Pacilio Senior Vice President, Exelon Generation Company, LLC President and Chief Nuclear Office (CNO), Exelon Nuclear 4300 Warrenville Road Warrenville, IL 60555 SUBJECT: BYRON STATION, UNITS 1 AND 2, NRC INTEGRATED INSPECTION REPORT 05000454/2011005; 05000455/2011005 Dear Mr. Pacilio: On December 31, 2011, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated inspection at your Byron Station, Units 1 and 2.  The enclosed inspection report documents the inspection findings which were discussed on January 12, 2012, with Mr. B. Youman and other members of your staff. The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license.  The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. Three NRC-identified findings of very low safety significance (Green) were identified during this inspection.  These findings were determined to involve violations of NRC requirements.  Further, a licensee-identified violation which was determined to be of very low safety significance is listed in this report.  The NRC is treating these violations as non-cited violations (NCVs) consistent with Section 2.3.2 of the NRC Enforcement Policy.   If you contest these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:  Document Control Desk, Washington, DC 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector Office at the Byron Station.  If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region III, and the NRC Resident Inspector at the Byron Station.    
{{#Wiki_filter:UNITED STATES
M. Pacilio     -2-  In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS).  ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). Sincerely,  /RA/  Eric R. Duncan, Chief Branch 3 Division of Reactor Projects Docket Nos. 50-454; 50-455 License Nos. NPF-37; NPF-66  Enclosure: Inspection Report No. 05000454/2011005 and 05000455/2011005    w/Attachment:  Supplemental Information cc w/encl: Distribution via ListServ  
NUCLEAR REGULATORY COMMISSION
Enclosure  U. S. NUCLEAR REGULATORY COMMISSION REGION III Docket Nos: 50-454; 50-455 License Nos: NPF-37; NPF-66 Report Nos: 05000454/2011005 and 05000455/2011005 Licensee: Exelon Generation Company, LLC Facility: Byron Station, Units 1 and 2 Location: Byron, IL Dates: October 1, 2011, through December 31, 2011 Inspectors: B. Bartlett, Senior Resident Inspector J. Robbins, Resident Inspector R. Ng, Project Engineer J. Dalzell-Bishop, DRS Emergency Response Specialist J. Cassidy, Senior Health Physicist R. Jickling, Senior Emergency Preparedness Inspector B. Palagi, Senior Operations Engineer J. Nance, Reactor Engineer  J. Benjamin, Braidwood Senior Resident Inspector C. Thompson, Resident Inspector, Illinois Emergency    Management Agency
REGION III
Approved by: E. Duncan, Chief Branch 3 Division of Reactor Projects         
2443 WARRENVILLE ROAD, SUITE 210
Enclosure  TABLE OF CONTENTS REPORT DETAILS .................................................................................................................... 4 Summary of Plant Status ........................................................................................................ 4 1R01 Adverse Weather Protection (71111.01) ............................................................ 4 1R04 Equipment Alignment (71111.04) ...................................................................... 5 1R05 Fire Protection (71111.05) ................................................................................. 6 1R11 Licensed Operator Requalification Program (71111.11) .................................... 7 1R12 Maintenance Effectiveness (71111.12) .............................................................. 8 1R13  Maintenance Risk Assessments and Emergent Work Control (71111.13) ......... 9 1R15 Operability Evaluations (71111.15) ...................................................................10 1R19 Post-Maintenance Testing (71111.19) ..............................................................17 1R20 Outage Activities (71111.20) ............................................................................18 2. REACTOR SAFETY ...................................................................................................20 1EP4 Emergency Action Level and Emergency Plan Changes (71114.04) ................20 1EP6 Drill Evaluation (71114.06) ...............................................................................21 3. RADIATION SAFETY .................................................................................................21 2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01) ..............21 2RS3 In-Plant Airborne Radioactivity Control and Mitigation (71124.03) ....................24 2RS4 Occupational Dose Assessment (71124.04) .....................................................25 2RS5 Radiation Monitoring Instrumentation (71124.05) .............................................26 2RS6 Radioactive Gaseous and Liquid Effluent Treatment (71124.06) ......................26 2RS7 Radiological Environmental Monitoring Program (71124.07) ............................32 2RS8 Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and Transportation (71124.08) ...........................................................................34 4. OTHER ACTIVITIES ...................................................................................................40 4OA1 Performance Indicator Verification (71151).......................................................40 4OA2 Identification and Resolution of Problems (71152)............................................45 4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153) ...............47 4OA6  Management Meetings .....................................................................................48 4OA7  Licensee-Identified Violations ...........................................................................48 SUPPLEMENTAL INFORMATION ............................................................................................. 1 Key Points of Contact ............................................................................................................. 1 List of Items Opened, Closed, and Discussed ........................................................................ 1 List Of Documents Reviewed.................................................................................................. 3 List Of Acronyms Used ..........................................................................................................13     
LISLE, IL 60532
1 Enclosure  SUMMARY OF FINDINGS Inspection Report (IR) 05000454/2011005, 05000455/2011005; 10/01/2011 - 12/31/2011; Byron Station, Units 1 & 2; Operability Evaluations and Functional Assessments; Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and Transportation This report covers a 3-month period of inspection by resident inspectors and announced baseline inspections by regional inspectors.  Three Green findings were identified by the inspectors.  The findings were considered Non-Cited Violations (NCVs) of NRC regulations.  The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP).  Assigned cross-cutting aspects were determined using IMC 0310, "Components Within the Cross-Cutting Areas."  Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006. A. Cornerstone:  Mitigating Systems NRC-Identified and Self-Revealed Findings Green.  The inspectors identified a finding of very low safety significance and an associated NCV of 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," when licensee personnel failed to identify voided piping between Unit 1 valves 1AF006B and 1AF017B and Unit 2 valves 2AF006B and 2AF017B of the auxiliary feedwater (AF) system.  The piping between these valves had been historically voided until they were recently re-designed to be filled and maintained filled with water to address an NRC-identified Green finding and an associated NCV of 10 CFR Part 50, Appendix B, Criterion III, "Design Control."  The licensee entered this issue into their Corrective Action Program (CAP) as IR 1296819, IR 1292337, and IR 1295760.  Corrective actions included instituting an Operations Standing Order, replacing the Unit 1 AF drain valve, and the isolation of the Unit 2 AF drain valve. This finding was determined to be more than minor because it was associated with the Design Control attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective of ensuring the availability, reliability and capability of systems  
-4352  February 7, 2012
that respond to initiating events to prevent undesirable consequences (i.e., core damage).  The inspectors determined that the finding could be evaluated using the SDP in accordance with IMC 0609, "Significance Determination Process," Attachment 0609.04, "Phase 1 - Initial Screening and Characterization of Findings," Table 4a for the Mitigating Systems Cornerstone. Specifically, the inspectors answered "Yes" to Question 1 - Is the finding a design or qualification deficiency confirmed not to result in a loss of operability or functionality? Based upon this Phase 1 screening, the inspectors concluded that the finding was of very low safety significance (Green).  This finding had a cross-cutting aspect in the Resources component of the Human Performance cross-cutting area [H.2(c)] because the licensee did not have adequate procedures to ensure that piping between Unit 1 valves 1AF006B and 1AF017B and Unit 2 valves 2AF006B and 2AF017B were maintained filled with water. (Section 1R15)  
  Mr. Michael J. Pacil
2 Enclosure  GreenThis finding was determined to be more than minor because it was associated with the Design Control attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage).  The inspectors determined that the finding could be evaluated using the SDP in accordance with IMC 0609, "Significance Determination Process," Attachment 0609.04, "Phase 1 - Initial Screening and Characterization of Findings," Table 4a, for the Mitigating Systems cornerstone.  Specifically, the inspectors answered "No" to all of the Mitigating Systems Cornerstone questions in Table 4a. Based upon this Phase 1 screening, the inspectors concluded that the finding was of very low safety significance (Green).  This finding had a cross-cutting aspect in the Corrective Action Program component of the Problem Identification and Resolution cross-cutting area [P.1(c)] because the licensee failed to thoroughly evaluate the impact on operability of a non-conforming condition associated with hazard barrier damper closure times.  (Section 1R15) .  The inspectors identified a finding of very low safety significance and an associated NCV of 10 CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," when licensee personnel failed to adhere to Operability Determination Process standards after identifying a non-conservative assumption related to closure times for hazard barrier dampers separating the Turbine Building from various safety-related rooms within the Auxiliary Building.  In particular, the issues raised by the inspectors during their review of Operability Evaluation 11-006, Revision 1, resulted in the station re-evaluating the non-conservative assumptions against aspects of the current licensing basis (CLB) not previously considered, and substantially revising the Operability Evaluation. The licensee entered these issues into their CAP as IR 1184258, IR 1237133, IR 1238611, IR 1240295, IR 1244251, and IR 1276895.  In addition to revising Operability Evaluation 2011-006, corrective actions included an assignment to reconstitute design basis calculation records and plans to re-design the hazard barrier dampers. Cornerstone:  Public Radiation Safety Green.  A self-revealed finding of very low safety significance and an associated NCV of 10 CFR 71.5, "Transportation of Licensed Material," was identified when licensee personnel failed to comply with 49 CFR 172.203(c) and shipped packages of radioactive material with transport manifests that did not document all applicable hazardous substances.  The issue was entered in the licensee's CAP as IR 1285148.  Immediate corrective actions included providing a corrected copy of the transport manifest to the waste processor.  Further, the licensee placed locks on the shipping containers to control items placed in the packages and to ensure that the manifest accurately represented the hazards contained in the shipping packages.  
i o Senior Vice President, Exelon Generation Company, LLC
This finding was determined to be more than minor because it was associated with the Program and Process attribute of the Public Radiation Safety Cornerstone and adversely affected the cornerstone objective of ensuring adequate protection of public health and safety from exposure to radioactive materials released into the public domain as a result  
President and Chief Nuclear Office (CNO), Exelon Nuclear
of routine civilian nuclear reactor operation, in that, providing incorrect information, as part of hazards communications, could impact the actions of response personnel.  The inspectors determined that the finding could be evaluated using the SDP in accordance with IMC 0609, "Significance Determination Process," Appendix D, "Public Radiation   
4300 Warrenville Road
3 Enclosure  Safety Significance Determination Process."  Using the Public Radiation Safety SDP, the inspectors determined:  (1) radiation limits were not exceeded; (2) there was no breach of a package during transit; (3) this issue did not involve a certificate of compliance; (4) this issue was not a low level burial ground nonconformance; and (5) this issue did not involve a failure to make notifications or provide emergency information.  As a result, the finding screened as having very low safety significance (Green).  This finding had a cross-cutting aspect in the Work Control component of the Human Performance cross-cutting area [H.3(b)] since the licensee failed to coordinate work activities by incorporating actions to address the impact of the work on different job activities, and the need for work groups to maintain interfaces with offsite organizations, and communicate, coordinate, and cooperate with each other during activities in which interdepartmental  
Warrenville, IL
coordination was necessary to assure adequate human performance.  Specifically, these events occurred because the licensee did not control the items placed in the waste packages and was not present when the boxes were loaded. (Section 2RS8)  B.      One violation of very low safety significance that was identified by the licensee has been reviewed by the inspectors.  Corrective actions planned or taken by the licensee have been entered into the licensee's CAP.  This violation and the associated corrective action tracking number are listed in Section 4OA7 of this report.  Licensee-Identified Violations    
  60555 SUBJECT: BYRON STATION, UNITS
4 Enclosure  REPORT DETAILS Unit 1 operated at or near full power from the beginning of the inspection period until November 11, 2011, when power was reduced to 89 percent to perform scheduled turbine throttle and governor valve testing.  The unit was returned to full power the following day and operated at full power for the remainder of the assessment period.  Summary of Plant Status Unit 2 began the inspection period shut down and in a planned refueling outage.  The unit was restarted and returned to service on October 10, 2011.  On November 5, 2011, reactor power was reduced to 96 percent to perform feedwater heater maintenance.  The unit was returned to full power on November 14, 2011, and operated at full power for the remainder of the inspection period. 1. REACTOR SAFETY Cornerstones:  Initiating Events, Mitigating Systems, Barrier Integrity and Emergency Preparedness 1R01 Adverse Weather Protection.1  (71111.01) a. Winter Seasonal Readiness Preparations The inspectors conducted a review of the licensee's preparations for winter conditions to verify that the plant's design features and implementation of procedures were sufficient to protect mitigating systems from the effects of adverse weather.  Documentation for selected risk-significant systems was reviewed to ensure that these systems would remain functional when challenged by inclement weather.  During the inspection, the inspectors focused on plant specific design features and the licensee's procedures used to mitigate or respond to adverse weather conditions.  Additionally, the inspectors reviewed the Updated Final Safety Analysis Report (UFSAR) and performance requirements for systems selected for inspection, and verified that operator actions were appropriate as specified by plant specific procedures.  Cold weather protection, such as heat tracing and area heaters, was verified to be in operation where applicable. The inspectors also reviewed Corrective Action Program (CAP) items to verify that the licensee was identifying adverse weather issues at an appropriate threshold and entering them into their CAP in accordance with station corrective action procedures. Specific documents reviewed during this inspection are listed in the Attachment.  The  
1 AND 2, NRC INTEGRATED INSPECTION REPORT 05000454/2011005; 05000455/2011005 Dear Mr. Pacilio
inspectors' reviews focused specifically on the following plant systems due to their risk significance or susceptibility to cold weather issues: Inspection Scope Station Heating System (SH); Auxiliary Building Heating, Ventilation, and Air-Conditioning (HVAC) [VA]; and  Refueling Water Storage Tanks (RWSTs).  This inspection constituted one winter seasonal readiness preparation sample as defined in Inspection Procedure (IP) 71111.01-05.   
: On December 31, 2011, the U.S. Nuclear Regulatory Commission (NRC) completed a
5 Enclosure  b. No findings were identified. Findings 1R04 Equipment Alignment.1  (71111.04) a. Quarterly Partial System Walkdowns The inspectors performed partial system walkdowns of the following risk-significant systems: Inspection Scope Unit 2 Train A Residual Heat Removal System Following Restoration to its Standby Line-Up;  Unit 2 Train B Essential Service Water (SX) with the Unit 2 Train A SX Out-of-Service (OOS);  Unit 2 Train B Auxiliary Feedwater (AF) with the Unit 2 Train A AF OOS; and  Unit 1 Train A AF with the Unit 1 Train B AF OOS. The inspectors selected these systems based on their risk significance relative to the Reactor Safety Cornerstones at the time they were inspected.  The inspectors attempted to identify any discrepancies that could impact the function of the system, and, therefore, potentially increase risk.  The inspectors reviewed applicable operating procedures, system diagrams, UFSAR, Technical Specification (TS) requirements, outstanding work  
n integrated inspection
at your Byron Station, Units 1 and 2.  The
enclosed inspection report documents the inspection findings which were discussed on
January 12, 2012
, with Mr. B. Youman and other members of your staff.
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license.  The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
Three NRC-identified
findings of very low safety significance (Green) were identified
during this inspection.  These findings were determined to involve violations of NRC requirements.  Further, a licensee-identified violation which was determined to be of very low safety significance is listed in this report.  The NRC is treating these violations as n
on-cited violations (NCVs) consistent with Section 2.3.2 of the NRC Enforcement Policy.
  If you contest these  
NCV s, you should provide a response
within 30 days of the date of this inspection report, with the basis for your denial, to
the U.S. Nuclear Regulatory Commission, ATTN:  Document Control Desk, Washington, DC 20555
-0001, with a
copy to the Regional Administrator, U.S. Nuclear Regulatory Commission  
- Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532
-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555
-0001; and the Resident Inspector Office at the Byron Station.  If you disagree with a cross
-cutting aspect assignment  
in this report, you should provide a response within 30 days of
the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region III, and the NRC Resident Inspector at the Byron Station.
   
M. Pacilio
    -2-  In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter , its enclosure, and your response (if any)
will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of
NRC's document system (ADAMS).  ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading
-rm/adams.html
(the Public Electronic Reading Room).
Sincerely,  /RA/  Eric R. Duncan, Chie f Branch 3 Division of Reactor Projects Docket Nos. 50
-454; 50-455 License Nos. NPF
-37; NPF-66  Enclosure:
Inspection Report No. 05000454/
2011005 and 05000455/
2011005    w/Attachment:  Supplemental Information
cc w/encl:
Distribution via ListServ
   
Enclosure  U. S. NUCLEAR REGULATORY COMMISSION
REGION III
Docket Nos:
50-454; 50-455 License Nos:
NPF-37; NPF-66 Report Nos:
05000454/2011005 and 05000455/
2011005 Licensee: Exelon Generation Company, LLC
Facility: Byron Station, Units 1 and 2
Location: Byron, IL Dates: October 1, 2011, through December
31, 2011 Inspectors:
B. Bartlett, Senior Resident Inspector
  J. Robbins, Resident Inspector
  R. Ng, Project Engineer
  J. Dalzell
-Bishop, DRS Emergency Response Specialist
  J. Cassidy, Senior Health Physicist
  R. Jickling, Senior Emergency Preparedness Inspector
  B. Palagi, Senior Operations Engineer
  J. Nance, Reactor Engineer  J. Benjamin, Braidwood Senior Resident Inspector
  C. Thompson, Resident Inspector, Illinois Emergency  
   Management Agency
 
Approved by:
E. Duncan, Chief Branch 3 Division of Reactor Projects         
Enclosure  TABLE OF CONTENTS
  REPORT DETAILS
................................................................................................
....................
4 Summary of Plant Status
................................................................................................
........ 4 1R01 Adverse Weather Protection (71111.01)
............................................................
4 1R04 Equipment Alignment (71111.04)
................................................................
...... 5 1R05 Fire Protection (71111.05)
................................................................
.................
6 1R11 Licensed Operator Requalification Program (71111.11)
................................
.... 7 1R12 Maintenance Effectiveness (71111.12)
..............................................................
8 1R13  Maintenance Risk Assessments and Emergent Work Control (71111.13)
......... 9 1R15 Operability Evaluations (71111.15)
...................................................................10 1R19 Post-Maintenance Testing (71111.19)
................................
..............................
17 1R20 Outage Activities (71111.20)
............................................................................
18 2. REACTOR SAFETY
................................................................................................
...20 1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)
................
20 1EP6 Drill Evaluation (71114.06)
................................................................
...............
21 3. RADIATION SAFETY
................................................................................................
.21 2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01)
..............
21 2RS3 In-Plant Airborne Radioactivity Control and Mitigation (71124.03)
....................
24 2RS4 Occupational Dose Assessment (71124.04)
.....................................................
25 2RS5 Radiation Monitoring Instrumentation (71124.05)
................................
.............
26 2RS6 Radioactive Gaseous and Liquid Effluent Treatment (71124.06)
......................
26 2RS7 Radiological Environmental Monitoring Program (71124.07)
............................
32 2RS8 Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and Transportation (71124.08)
...........................................................................
34 4. OTHER ACTIVITIES
................................................................................................
...40 4OA1 Performance Indicator Verification (71151)
................................
.......................
40 4OA2 Identification and Resolution of Problems (71152)
................................
............
45 4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153)
...............
47 4OA6  Management Meetings
.....................................................................................
48 4OA7  Licensee-Identified Violations
...........................................................................
48 SUPPLEMENTAL INFORMATION
.............................................................................................
1 Key Points of Contact
................................................................
................................
.............
1 List of Items Opened, Closed, and Discussed
................................................................
........ 1 List Of Documents Reviewed
................................................................................................
.. 3 List Of Acronyms Used
................................................................................................
..........
13     
1 Enclosure  SUMMARY OF FINDINGS
Inspection Report (IR) 05000454/2011005, 05000455/2011005; 10/01/2011  
- 12/31/2011;
Byron Station, Units 1 &
2; Operability Evaluations
and Functional Assessments; Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and Transportation
This report covers a  
3-month period of inspection by resident inspectors and announced baseline inspections by regional inspector
s.  Three Green findings were identified by the inspectors.  The findings were considered Non-Cited Violation
s (NCVs) of NRC regulations.  The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP).  Assigned cross-cutting aspects were determined using IMC
0310, "Components Within the Cross
-Cutting Areas."  Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review.
  The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG
-1649, "Reactor Oversight Process," Revision 4, dated December 2006.
A. Cornerstone:  Mitigating Systems
NRC-Identified and Self
-Revealed Findings
Green.  The inspectors identified a finding of very low safety significance and an associated NCV of 10 CFR Part 50, Appendix B, Criterion
XVI, "Corrective Action," when licensee personnel failed to identify voided piping between Unit 1 valves 1AF006B and 1AF017B and Unit 2 valves 2AF006B and 2AF 017B of the auxiliary feedwater (AF) system.  The piping between these valves had been historically voided until they were recently re
-design ed to be filled and maintained filled with water to address a
n NRC-identified Green
finding and an associated NCV of 10 CFR Part 50, Appendix B, Criterion III, "Design Control
."  The licensee entered this issue into their Corrective Action Program (CAP) as IR 1296819, IR 1292337, and IR 1295760.  Corrective actions include d instituting  
an Operations Standing Order, replacing the Unit 1 AF drain valve, and the isolation of the Unit 2 AF drain valve.
  This finding was determined to be more than minor because it was associated with th
e Design Control attribute of the Mitigating Systems  
Cornerstone  
and adversely affected the cornerstone objective of ensuring the availability, reliability and capability of systems  
that respond to initiating events to prevent undesirable consequences (i.e., core damage).  The inspectors determined that the finding could be evaluated using the SDP in accordance with IMC 0609, "Significance Determination Process," Attachment
0609.04, "Phase 1  
- Initial Screening and Characterization of Findings," Table 4a for the Mitigating
Systems Cornerstone.
  Specifically, the inspectors answered "Y es" to Question 1  
- Is the finding a design or qualification deficiency confirmed not to result in a loss of operability or functionality?
  Based upon this Phase 1 screening, the inspectors concluded that the finding was of very low safety significance (Green).  This finding had a cross-cutting aspect in t
he Resources component of the
Human Performance cross
-cutting area [H.2(c)] because the licensee did not have adequate procedures to ensure that piping between Unit 1 valves 1AF006B and 1AF017B and Unit 2 valves 2AF006B and 2AF017B were maintained filled with water. (Section 1R15)
 
2 Enclosure  GreenThis finding was determined to be more than minor
because it was associated with the Design Control attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective of ensuring
the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage).  The inspectors determined that the finding could be evaluated using the SDP in accordance with IMC 0609, "Significance Determination Process," Attachment
0609.04, "Phase 1  
- Initial Screening and Characterization of Findings," Table 4a, for the Mitigating Systems cornerstone.  Specifically, the inspectors answered "No" to all of the Mitigating Systems Cornerstone questions in Table 4a.
  Based upon this Phase 1 screening, the inspectors concluded that the finding was of very low safety significance (Green).  This finding had
a cross-cutting aspect in the Corrective Action Program component of the Problem Identification and Resolution cross-cutting area [P.1(c)] because
the licensee failed to thoroughly evaluate the impact on operability of a  
non-conforming condition associated with hazard barrier damper closure times.  (Section 1R15) .  The inspectors identified a finding of very low safety significance and an associated NCV of 10 CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," when licensee personnel failed to adhere to  
Operability Determination Process standards after identifying a non
-conservative assumption related to closure times for hazard barrier dampers separating the Turbine Building from various safety
-related rooms within the Auxiliary Building.  In particular, the issues raised by the inspectors during their review of Operability Evaluation  
11-006, Revision 1, resulted in the station  
re-evaluating the non
-conservative assumptions against aspects of the current licensing basis (CLB) not previously considered, and substantially revising the Operability Evaluation.
  The licensee entered these issues into their CAP as IR 1184258, IR 1237133, IR 1238611, IR 1240295, IR 1244251, and IR
1276895.  In addition to revising Operability Evaluation 2011
-006, corrective actions included an assignment
to reconstitute  
design basis calculation records and plans to re
-design the hazard barrier dampers. Cornerstone:  Public Radiation Safety
Green.  A self-revealed finding of very low safety significance and an associated  
NCV of 10 CFR 71.5, "Transportation of
Licensed Material," was identified when licensee personnel failed to comply with 49 CFR 172.203(c) and shipped packages of radioactive material with transport manifest
s that did not document all applicable hazardous substances.  The issue
was entered in the licensee's CAP as IR 1285148.   
Immediate corrective actions included providing
a corrected copy of the transport manifest to the waste processor.  Further, the licensee placed locks on the shipping containers to control items placed in the packages and to ensure that the manifest accurately represented the hazards contained in the shipping packages.
 
This finding was determined to be more than minor because it was associated with the Program and Process attribute of the Public Radiation Safety  
Cornerstone  
a nd adversely affected the cornerstone objective
of ensuring adequate protection of public health and safety from exposure to radioactive materials released into the public domain as a result  
of routine civilian nuclear reactor operation, in that, providing
incorrect information, as part of hazard
s communication
s, could impact the actions of response personnel.  The inspectors determined that the finding could be evaluated using the SDP in accordance with IMC 0609, "Significance Determination Process," Appendix D, "Public Radiation   
3 Enclosure  Safety Significance Determination Process."  Using the Public Radiation Safety SDP, the inspectors determined
:  (1) radiation limits were not exceeded; (2) there was no breach of a package during transit; (3) this issue
did not involve a certificate of compliance
; (4) this issue was not a low level burial ground nonconformance; and (5) this issue
did not involve a failure to make notifications or provide emergency information.  
  As a result, the finding screened as having very low safety significance (Green).  This finding had
a cross-cutting aspect in the Work Control component
of the Human Performance cross-cutting area [H.3(b)] since the licensee failed to coordinate work activities by incorporating actions to address the impact of
the work on different job activities, and the need for work groups to maintain interfaces with offsite organizations, and communicate, coordinate, and cooperate with each other during activities in which interdepartmental  
coordination was necessary to assure adequate human performance
.  Specifically, these events occurred because the licensee did not control the items
placed in the waste packages and was not present when the boxes were loaded.
  (Section 2RS8)  
  B.      One violation of very
low safety significance that was
identified by the licensee has been reviewed by the inspectors.  
  Corrective actions planned or taken by the licensee have been entered into the licensee's CAP.  This violation and the associated corrective
action tracking number
are listed in Section 4OA7 of this report.  
  Lic ensee-Identified Violations
   
4 Enclosure  REPORT DETAILS
Unit 1 operated at or near full power from the beginning of the inspection period until November 11, 2011, when power was reduced to 89 percent  
to perform scheduled turbine throttle and governor valve testing.  The unit was returned to full power the following day
and operated at full power for the remainder of the assessment period.  Summary of Plant Status
Unit 2 began the inspection period shut down and in a planned refueling outage.  The unit was restarted and returned to service on October 10, 2011.  On November 5, 2011, reactor power was reduced to 96 percent to perform feedwater heater maintenance.  The unit was returned to full power on November 14, 2011
, and operated at full power for the remainder of the inspection period. 1. REACTOR SAFETY
Cornerstones:  Initiating Events, Mitigating Systems, Barrier Integrity and Emergency Preparedness
1R01 Adverse Weather Protection
.1  (71111.01)
a. Winter Seasonal Readiness Preparations
The inspectors conducted a review of the licensee's preparations for winter conditions to verify that the plant's design features and implementation of procedures were sufficient to protect mitigating systems from the effects of adverse weather.  Documentation for selected risk
-significant systems was reviewed to ensure that these systems would remain functional when challenged by inclement weather.  During the inspection, the inspectors focused on plant specific design features and the licensee's procedures used to mitigate or respond to adverse weather conditions.  Additionally, the inspectors reviewed the Updated Final Safety Analysis Report (UFSAR) and performance requirements for systems selected for inspection, and verified that operator actions were appropriate as specified by plant specific procedures.  Cold weather protection, such as heat tracing and area heaters, was verified to be in operation where applicable.
  The inspectors also reviewed Corrective Action Program (CAP) items to verify that the licensee was identifying adverse weather issues at an appropriate threshold and entering them into their CAP in accordance with station corrective action procedures. Specific documents reviewed during this inspection are listed in the Attachment.  The  
inspectors' reviews focused specifically on the following plant systems due to their risk significance or susceptibility to cold weather issues:
Inspection Scope
  Station Heating System (SH);
  Auxiliary Building Heating, Ventilation, and Air
-Conditioning (HVAC) [VA]; and  Refueling Water Storage Tanks
(RWST s).  This inspection constituted
one winter seasonal readiness
preparation
sample as defined in Inspection Procedure (IP) 71111.01-05.   
5 Enclosure  b. No findings were identified.
Findings 1R04 Equipment Alignment
.1  (71111.04)
a. Quarterly Partial System Walkdowns
The inspectors performed partial system walkdowns of the following risk
-significant systems: Inspection Scope
  Unit 2 Train A Residual Heat Removal System Following Restoration to its Standby Line-U p;  Unit 2 Train B Essential Service Water (SX) with the Unit 2 Train A SX Out-of-Service (OOS);  Unit 2 Train B
Auxiliary Feedwater (AF) with the Unit 2 Train A AF OOS; and  Unit 1 Train A AF with the Unit 1 Train B AF OOS
. The inspectors selected these systems
based on their risk significance relative to the  
Reactor Safety Cornerstones at the time they were inspected.  The inspectors attempted to identify any discrepancies that could impact the function of the system, and, therefore, potentially increase risk.  
  The inspectors reviewed applicable operating procedures, system diagrams, UFSAR, Technical Specification (TS) requirements, outstanding work  
orders (WOs), condition reports, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have rendered the systems  
orders (WOs), condition reports, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have rendered the systems  
incapable of performing their intended functions.  The inspectors also walked down accessible portions of the systems to verify system components and support equipment were aligned correctly and operable.  The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no obvious deficiencies.  The inspectors also verified that the licensee had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the CAP with the appropriate significance characterization.  Documents reviewed are listed in the Attachment. These activities constituted four partial system walkdown samples as defined in IP 71111.04-05. b. No findings were identified. Findings   
incapable of performing their intended functions.  The inspectors also walked down accessible portions of the systems to verify system components and support equipment were aligned correctly and operable.  The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no obvious deficiencies.  The inspectors also verified that the licensee had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the CAP with the appropriate significance characterization.  Documents reviewed are listed in the  
6 Enclosure  1R05 Fire Protection.1  (71111.05) Routine Resident Inspector Toursa.  (71111.05Q) The inspectors conducted fire protection walkdowns which were focused on availability, accessibility, and the condition of firefighting equipment in the following risk-significant plant areas: Inspection Scope Unit 1 426' Turbine Building (Fire Zone 8.5-1);  Unit 1 426' Turbine Building (Fire Zone 8.5-1);  Unit 1 Train B Auxiliary Feedwater Pump Room (Fire Zone 11.4A-1); and  Unit 2 Train B Auxiliary Feedwater Pump Room (Fire Zone 11.4A-2 ). The inspectors reviewed areas to assess if the licensee had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant, effectively maintained fire detection and suppression capability, maintained passive fire protection features in good material condition, and implemented adequate compensatory measures for out-of-service, degraded or inoperable fire protection equipment, systems, or features in accordance with the licensee's fire plan.  The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plant's Individual Plant Examination of External Events with later additional insights, their potential to impact equipment which could initiate or mitigate a plant transient, or their impact on the plant's ability to respond to a security event.  Using the documents listed in the Attachment, the inspectors verified that fire hoses and extinguishers were in their designated locations and available for immediate use; that  
Attachment. These activities constituted four partial system walkdown samples as defined in  
fire detectors and sprinklers were unobstructed; that transient material loading was within the analyzed limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory condition.  The inspectors also verified that minor issues identified during the inspection were entered into the licensee's CAP.  Documents reviewed are listed in the Attachment. These activities constituted four quarterly fire protection inspection samples as defined in  
IP 71111.04-05. b. No findings were identified.
IP 71111.05-05. b. No findings were identified. Findings .2 Annual Fire Protection Drill Observationa.  (71111.05A) On November 11, 2011, and December 17, 2011, the inspectors observed a fire brigade activation Fire Drill in the Unit 1 Auxiliary Boiler Room, 401' Elevation (Fire Zone 8.3-1 SE).  Based on this observation, the inspectors evaluated the readiness of the plant fire brigade to fight fires.  The inspectors verified that the licensee staff identified deficiencies; openly discussed them in a self-critical manner at the drill debrief, and took appropriate corrective actions.  Specific attributes evaluated were: Inspection Scope
Findings   
7 Enclosure  proper wearing of turnout gear and self-contained breathing apparatus;  proper use and layout of fire hoses; employment of appropriate fire fighting techniques; sufficient firefighting equipment brought to the scene; effectiveness of fire brigade leader communications, command, and control; search for victims and propagation of the fire into other plant areas; smoke removal operations; utilization of pre-planned strategies; adherence to the pre-planned drill scenario; and drill objectives.   Documents reviewed are listed in the Attachment to this report. These activities constituted one annual fire protection inspection sample as defined in IP 71111.05-05. b. No findings were identified. Findings 1R11 Licensed Operator Requalification Program.1  (71111.11) Annual Operating Test Resultsa.  (71111.11B) The inspectors reviewed the overall pass/fail results of the Annual Operating Test,  
6 Enclosure  1R05 Fire Protection
administered by the licensee from October 18, 2011 through December 8, 2011, required by 10 CFR 55.59(a).  The results were compared to the thresholds established in IMC 0609, Appendix I, "Licensed Operator Requalification Significance Determination Process (SDP)," to assess the overall adequacy of the licensee's Licensed Operator Requalification Program (LORT) to meet the requirements of 10 CFR 55.59. Inspection Scope This inspection constitutes one biennial and one annual licensed operator requalification inspection sample as defined in IP 71111.11B and IP71111.11A. b. No findings were identified. Findings .2 Resident Inspector Quarterly Reviewa.  (71111.11Q) On November 16, 2011, the inspectors observed a crew of licensed operators in the plant's simulator during licensed operator requalification examinations to verify that operator performance was adequate, evaluators were identifying and documenting crew performance problems and training was being conducted in accordance with licensee procedures.  The inspectors evaluated the following areas: Inspection Scope  
.1  (71111.05)
8 Enclosure  licensed operator performance; crew's clarity and formality of communications; ability to take timely actions in the conservative direction; prioritization, interpretation, and verification of annunciator alarms; correct use and implementation of abnormal and emergency procedures; control board manipulations; oversight and direction from supervisors; and ability to identify and implement appropriate TS actions and emergency plan actions and notifications. The crew's performance in these areas was compared to pre-established operator action expectations and successful critical task completion requirements. Documents reviewed are listed in the Attachment. In addition, the inspectors observed licensed operator performance in the actual plant and the main control room during this calendar quarter. This inspection constituted one quarterly licensed operator requalification program sample as defined in IP 71111.11. b. No findings were identified. Findings 1R12 Maintenance Effectiveness.1  (71111.12) Routine Quarterly Evaluationsa.  (71111.12Q) The inspectors evaluated degraded performance issues involving the following risk-significant systems: Inspection Scope Unit 1 Rod Drive Motor Generator (MG) Set High Vibrations; and  High Energy Line Break (HELB) Dampers. The inspectors reviewed events including those in which ineffective equipment maintenance had resulted in valid or invalid automatic actuations of engineered safeguards systems and independently verified the licensee's actions to address system performance or condition problems in terms of the following: implementing appropriate work practices; identifying and addressing common cause failures; scoping of systems in accordance with 10 CFR 50.65(b) of the Maintenance Rule;  characterizing system reliability issues for performance; charging unavailability for performance; trending key parameters for condition monitoring; ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and verifying appropriate performance criteria for structures, systems, and components (SSCs)/functions classified as (a)(2) or appropriate and adequate  goals and corrective actions for systems classified as (a)(1).
Routine Resident Inspector Tours
9 Enclosure  The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the system.  In addition, the inspectors verified maintenance effectiveness issues were entered into the CAP with the appropriate significance characterization.  Documents reviewed are listed in the Attachment. This inspection constituted two quarterly maintenance effectiveness sample as defined in IP 71111.12-05. b. No findings were identified. Findings 1R13  Maintenance Risk Assessments and Emergent Work Control.1  (71111.13) a. Maintenance Risk Assessments and Emergent Work Control The inspectors reviewed the licensee's evaluation and management of plant risk for the maintenance and emergent work activities affecting risk-significant and safety-related equipment listed below to verify that the appropriate risk assessments were performed prior to removing equipment for work: Inspection Scope Shutdown Safety Associated with Cavity Drain;  Unit Common B Fire Pump OOS With SX as its Backup While One Train of SX was OOS;  Review of Planned Risk Significant Activities During Elevated Winds and Low River Level; and  Unit 2 Train B Auxiliary Feedwater Pump OOS. These activities were selected based on their potential risk significance relative to the Reactor Safety Cornerstones.  As applicable for each activity, the inspectors verified that risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate and complete.  When emergent work was performed, the inspectors verified that the plant risk was promptly reassessed and managed.  The inspectors reviewed the scope of maintenance work, discussed the results of the assessment with the licensee's  
a.  (71111.05Q)
The inspectors conducted fire protection walkdowns which were focused on availability, accessibility, and the condition of firefighting equipment in the following risk
-significant plant areas:
Inspection Scope
  Unit 1 426
' Turbine Building (Fire Zone 8.5
-1);  Unit 1 426
' Turbine Building (Fire Zone 8.5-1);  Unit 1 Train B Auxiliary Feedwater Pump Room (Fire Zone 11.4A
-1); and  Unit 2 Train B Auxiliary Feedwater Pump Room (Fire Zone 11.4A
-2 ). The inspectors reviewed areas to assess if the licensee had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant, effectively maintained fire detection and suppression capability, maintained passive fire protection features in good material condition, and implemented adequate compensatory measures for out
-of-service, degraded or inoperable fire protection equipment, systems, or features in accordance with the licensee's fire plan.  The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plant's Individual Plant Examination of External Events with later additional insights, their potential to impact equipment which could initiate or mitigate a plant transient, or their impact on the plant's ability to respond to a security event.  Using the documents listed in the Attachment, the inspectors verified that fire hoses and extinguishers were in their designated locations and available for immediate use; that  
fire detectors and sprinklers were unobstructed;
that transient material loading was within the analyzed limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory condition.  The inspectors also verified that minor issues identified during the inspection were entered into the licensee's CAP.  Documents reviewed are listed in the Attachment
. These activities constituted four quarterly fire protection inspection samples as defined in  
 
IP 71111.05-05. b. No findings were identified.
Findings .2 Annual Fire Protection Drill Observation
a.  (71111.05A)
On November 11, 2011 , and December 17, 2011, the inspectors observed a fire brigade activation Fire Drill in the Unit 1 Auxiliary Boiler Room, 401' Elevation (Fire Zone 8.3
-1 SE).  Based on this
observation, the inspectors
evaluated the readiness of the plant
fire brigade to fight fires.  The inspectors verified that the licensee staff identified deficiencies; openly discussed them in a self
-critical manner at the drill debrief, and took appropriate corrective actions.  Specific attributes evaluated were:
Inspection Scope
 
7 Enclosure  proper wearing of turnout gear and self
-contained breathing apparatus;  
   proper use and layout of fire hoses;
  employment of appropriate fire fighting techniques;
  sufficient firefighting equipment brought to the scene;
  effectiveness of fire brigade leader communications, command, and control;
  search for victims and propagation of the fire into other plant areas;
  smoke removal operations;
  utilization of pre
-planned strategies;
  adherence to the pre
-planned drill scenario; and
  drill objectives.
  Documents reviewed
are listed in the Attachment to this report.
These activities constituted one annual fire protection inspection sample as defined in  
IP 71111.05-05. b. No findings were identified.
Findings 1R11 Licensed Operator Requalification Program
.1  (71111.11)
Annual Operating Test Results
a.  (71111.11B)
The inspectors reviewed the overall pass/fail results of the Annual Operating Test,  
administered by the licensee from October 18, 2011
through December 8, 2011, required by 10
CFR 55.59(a).  The results were compared to the thresholds established in IMC 0609, Appendix I, "Licensed Operator Requalification Significance Determination Process (SDP)," to assess the overall adequacy of the licensee's Licensed Operator Requalification Program (LORT) to meet the requirements of  
10 CFR 55.59. Inspection Scope
This inspection constitutes one biennial
and one annual
licensed operator requalification inspection sample as defined in IP
71111.11B and IP71111.11A
. b. No findings were identified.
Findings .2 Resident Inspector Quarterly Review
a.  (71111.11Q)
On November 16, 2011, the inspectors observed a crew of licensed operators in the plant's simulator during licensed operator requalification examinations to verify that operator performance was adequate, evaluators were identifying and documenting crew performance problems and training was being conducted in accordance with licensee procedures.  The inspectors evaluated the following areas:
Inspection Scope
 
8 Enclosure  licensed operator performance;
  crew's clarity and formality of communications;
  ability to take timely actions in the conservative direction;
  prioritization, interpretation, and verification of annunciator alarms;
  correct use and implementation of abnormal and emergency procedures;
  control board manipulations;
  oversight and direction from supervisors; and
  ability to identify and implement appropriate TS actions and  
emergency plan actions and notifications.
The crew's performance in these areas was compared to pre
-established operator action expectations and successful critical task completion requirements.
  Documents reviewed are listed in the Attachment.
In addition, the inspectors observed licensed operator performance in the actual plant and the main control room during this calendar quarter.
This inspection constituted one
quarterly licensed operator requalification program sample as defined in IP
71111.11. b. No findings were identified.
Findings 1R12 Maintenance Effectiveness
.1  (71111.12)
Routine Quarterly Evaluations
a.  (71111.12Q)
The inspectors evaluated degraded performance
issues involving the following
risk-significant systems:
Inspection Scope
  Unit 1 Rod Drive Motor Generator (MG) Set High Vibrations; and  High Energy Line Break (HELB) Dampers.
The inspectors reviewed events
including those in which
ineffective equipmen
t maintenance had
resulted in valid or invalid automatic actuations of  
engineered  
safeguards  
systems and independently verified the licensee's actions to address system performance or condition problems in terms of the following:
  implementing appropriate work practices;
  identifying and addressing common cause failures;
  scoping of systems in accordance with  
10 CFR 50.65(b) of the Maintenance Rule;  characterizing system reliability issues for performance;
  charging unavailability for performance;
  trending key parameters for condition monitoring;
  ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re
-classification; and
  verifying appropriate performance criteria for structures, systems, and
  components (SSCs)/functions classified as (a)(2) or appropriate and
adequate  goals and corrective actions for systems classified as (a)(1).
 
9 Enclosure  The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the system.  In addition, the inspectors verified maintenance effectiveness issues were entered into the CAP with the appropriate significance characterization.  Documents reviewed are listed in the  
Attachment.
This inspection constituted two quarterly maintenance effectiveness sample as defined in IP 71111.12-05. b. No findings were identified.
Findings 1R13  Maintenance Risk Assessments and Emergent Work Control
.1  (71111.13)
a. Maintenance Risk Assessments and Emergent Work Control
The inspectors reviewed the licensee's evaluation and management of plant risk for the maintenance and emergent work activities affecting risk
-significant and safety
-related equipment listed below to verify that the appropriate risk assessments were performed prior to removing equipment for work:
Inspection Scope
  Shutdown Safety Associated with Cavity Drain
;  Unit Common B Fire Pump OOS With SX as its Backup While O
ne Train of SX was OOS;  Review of Planned Risk Significant Activities During Elevated Winds and Low River Level; and  Unit 2 Train B Auxiliary Feedwater Pump OOS. These activities were selected based on their potential risk significance relative to the  
Reactor Safety Cornerstones.  As applicable for each activity, the inspectors verified that risk assessments were performed as required by  
10 CFR 50.65(a)(4) and were accurate and complete.  When emergent work was performed, the inspectors verified that the plant risk was promptly reassessed and managed.  The inspectors reviewed the scope of maintenance work, discussed the results of the assessment with the licensee's  
probabilistic risk analyst or shift technical advisor, and verified plant conditions were consistent with the risk assessment.  The inspectors also reviewed TS requirements and walked down portions of redundant safety systems, when applicable, to verify risk  
probabilistic risk analyst or shift technical advisor, and verified plant conditions were consistent with the risk assessment.  The inspectors also reviewed TS requirements and walked down portions of redundant safety systems, when applicable, to verify risk  
analysis assumptions were valid and applicable requirements were met. These maintenance risk assessments and emergent work control activities constituted four samples as defined in IP 71111.13-05. b. No findings were identified. Findings   
analysis assumptions were valid and applicable requirements were met.
10 Enclosure  1R15 Operability Evaluations.1  (71111.15) a. Operability Evaluations The inspectors reviewed the following issues: Inspection Scope Unit 1 Embedment Plate 1SI06025V Due to Questions Regarding Supporting Analysis/Calculations;  Unit 1 Seismic Support 1FW01147X Due to Questions Regarding Impact to HELB Analysis;  Unit 1 and Unit 2 Train B AF Pumps Due to Questions Regarding Multiple Starts;  Unit 1 Leading Edge Flow Monitor Due to Identified Anomaly in Trended Data;  Unit 1 and Unit 2 Train B AF Pumps Due to Potential Pipe Voids in Cross-Tie Piping; and  Unit 1 Engineered Safety Features Switchgear Rooms Division 11 and 12 Due to Questions Regarding 1VX20Y and 1VX17Y Fire Damper "S" Hooks Preventing Closure of Dampers The inspectors selected these potential operability issues based on the risk significance of the associated components and systems.  The inspectors evaluated the technical adequacy of the evaluations to ensure that TS operability was properly justified and the  
These maintenance risk assessments and emergent work control activities constituted four samples as defined in IP
71111.13-05. b. No findings were identified.
Findings   
10 Enclosure  1R15 Operability Evaluations
.1  (71111.15)
a. Operability Evaluations
The inspectors reviewed the following issues:
Inspection Scope
  Unit 1 Embedment Plate 1SI06025V Due to Questions Regarding Supporting Analysis/Calculations
;  Unit 1 Seismic Support 1FW01147X Due to Questions Regarding Impact to HELB Analysis;  Unit 1 and Unit 2 Train B AF
Pump s Due to Questions Regarding Multiple Starts
;  Unit 1 Leading Edge Flow Monitor Due to Identified Anomaly in Trended Data
;  Unit 1 and Unit 2 Train B A
F Pump s Due to Potential Pipe Voids in Cross
-Tie Piping; and  Unit 1 Engineered Safety Features Switchgear Rooms Division 11 and 12 Due to Questions Regarding 1VX20Y and 1VX17Y Fire Damper "S" Hooks Preventing Closure of Dampers
The inspectors selected these potential operability issues based on the risk
significance of the associated components and systems.  The inspectors evaluated the
technical adequacy of the evaluations to ensure that TS operability was properly justified and the  
subject component or system remained available such that no unrecognized increase in  
subject component or system remained available such that no unrecognized increase in  
risk occurred.  The inspectors compared the operability and design criteria in the appropriate sections of the TS and UFSAR to the licensee's evaluations to determine whether the components or systems were operable.  Where compensatory measures were required
risk occurred.  The inspectors compared the operability and design criteria in the appropriate sections of the
TS and U FSAR to the licensee's evaluations to determine whether the components or systems were operable.  Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled.  The inspectors determined, where appropriate, compliance with bounding limitations associated with the evaluations.  Additionally, the inspectors reviewed a sample of corrective action documents to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations.
  Documents reviewed are listed in the
Attachment.
This operability inspection constituted six
samples as defined in IP
71111.15-0 5. b.      .1) Findings Failure to Identify Auxiliary Feedwater Pump Suction
Voids  Introduction
:  The inspectors identified a finding of very low safety significance (Green)
and an associated NCV of 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," when licensee personnel failed to identify voided piping between Unit 1 valves 1AF006B and 1AF017B and Unit 2 valves
2AF006B and 2AF017B of the auxiliary feedwater system.
  The piping between these valves had been historically voided until they were recently re
-design ed to be filled and maintained filled with water to address a
n NRC-identified Green finding and an associated NCV of 10 CFR Part 50, Appendix B, Criterion III, "Design Control"
(NCV 05000454/2011004
-04; 05000455/
-2011004-04, Design of Auxiliary Feedwater System Included Voids in Safety
-Related Alternate Suction Flow Paths)
11 Enclosure  DescriptionOn November 17, 2011, the inspectors reviewed the Inspection Reports (I
Rs) generated
the previous day and
did not identify
any that documented the issue discussed above.  The inspectors
re-inspected the tygon tubing between Unit 1 valves 1AF006B and 1AF017B and Unit 2 valves 2AF006B and
2AF017B and could not determine whether there was water in the tygon tubi ng. Licensee management was subsequently notified of the inspector's observations
.  The licensee performed a system walkdown and confirmed that there was no visible wate r level in the tygon tubing
between Unit 1 valves 1AF006B and
1AF017B.  The section of piping between the valves was subsequently filled with water and verified full through
ultrasonic testing.
:  On November
16, 2011, the inspectors notified licensee staff that there appeared to be no visible water in tygon tubing attached to vent valves between Unit 1 valves 1AF006B and
1AF017B and Unit 2 valves
2AF006B and
2AF017B.  Visible water in tygon tubing attached to these vent valves was being used as an indication that the piping between these valves was filled with water.  The inspectors could not determine whether there was water
Special attention was made to identify potential unmonitored release points (such as open roof vents in boiling water reactor turbine decks, temporary structures butted against turbine, auxiliary or containment buildings), building alterations which could impact airborne or liquid effluent controls, and ventilation system leakage that  
Special attention was made to identify potential unmonitored release points (such as open roof vents in boiling water reactor turbine decks, temporary structures butted against turbine, auxiliary or containment buildings), building alterations which could impact airborne or liquid effluent controls, and ventilation system leakage that  
communicated directly with the environment. Inspection Scope For equipment or areas associated with the systems selected for review that were not readily accessible due to radiological conditions, the inspectors reviewed the licensee's material condition surveillance records, as applicable.
communicated
directly with the environment.
Inspection Scope
For equipment or areas associated with the systems selected for review that were not readily accessible due to radiological conditions, the inspectors reviewed the licensee's material condition surveillance records, as applicable.
The inspectors walked down filtered
-ventilation systems to assess for conditions such as degraded high-efficiency particulate air/charcoal banks, improper alignment, or system installation issues that would impact the performance or the effluent monitoring capability of the effluent system.
As available, the inspectors observed selected portions of the routine processing and discharge of radioactive gaseous effluent (including sample collection and analysis) to evaluate whether appropriate treatment equipment was used and the processing activities align
ed with discharge permits.
The inspectors determined if the licensee had
made significant changes to their effluent release points (e.g., changes subject to a 10 CFR 50.59 review or requiring
NRC approval of alternate discharge points
). As available, the inspectors observed selected portions of the routine processing and
discharge of liquid waste (including sample collection and analysis) to determine if appropriate effluent treatment equipment was being used and whether
radioactive liquid waste was being processed and discharged in accordance with procedure requirements
and aligned with discharge permits.
b. No findings were identified.
Findings 
29 Enclosure  .3 Sampling and Analyses
a.  (02.03) The inspectors selected effluent sampling activities, consistent with smart sampling, and assessed whether adequate controls had
been implemented to ensure representative samples were obtained (e.g.
, provisions for sample line flushing, vessel recirculation, composite samplers, etc.)
Inspection Scope
The inspectors selected effluent discharges made with inoperable (declared out
-of-service) effluent radiation monitors to assess whether controls were in place to ensure compensatory sampling
coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance.  The inspectors also reviewed the licensee's issue report database to determine if any problems had been identified with the PI data collected or transmitted  
coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance.  The inspectors also reviewed the licensee's issue report database to determine if any problems had been identified with the PI data collected or transmitted  
for this indicator.  Documents reviewed are listed in the Attachment. Inspection Scope This inspection constituted two MSPI high pressure injection system samples as defined in IP 71151-
for this indicator.  Documents reviewed
are listed in the Attachment.
Inspection Scope
This inspection constituted two MSPI high pressure injection system samples as defined in IP 71151-05. b. No findings were identified.
Findings 
44 Enclosure  .8 a. Occupational Exposure Control Effectiveness
The inspectors sampled licensee submittals for the occupational radiological occurrences PI for the period from the fourth quarter of 2010 through the 3rd
quarter of 2011.  To determine the accuracy of the PI data reported during these periods, t
he inspectors used PI definitions and guidance contained in NEI 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 6, dated October 2009.  The inspectors reviewed the licensee's assessment of the PI for occupational radiation safety to determine if indicator
-related data was adequately assessed and reported.  To assess the adequacy of the licensee's PI data collection and analyses, the inspectors discussed with radiation protection staff, the scope
, and breadth of its data review and the results
of those reviews.  The inspectors independently reviewed electronic personal dosimetry dose rate and accumulated dose alarms and dose reports and the dose assignments for any intakes that occurred during the time period reviewed to determine if there were
potentially unrecognized occurrences.  The inspectors also conducted walkdowns of numerous locked high and very high radiation area entrances to determine the adequacy of the controls in place for these areas.  Documents reviewed are listed in the Attachment. Inspection Scope
This inspection constituted one occupational exposure control effectiveness sample as defined in IP
71151-05. b. No findings were identified.
Findings .9 a. Radiological Effluent Technical Specification/Offsite Dose Calculation Manual Radiological Effluent Occurrences The inspectors sampled licensee submittals for the radiological effluent TS/ODCM
radiological effluent occurrences PI for the period from the fourth quarter of 2010 through the third quarter of 2011.  To determine the accuracy of the PI data reported during these periods, the inspectors used PI definitions and guidance contained in NEI 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 6, dated October 2009.  The inspectors reviewed the licensee's issue report
database and selected individual reports generated since this indicator was last reviewed to identify any potential occurrences such as unmonitored, uncontrolled, or improperly calculated effluent releases that may have impacted offsite dose.  The inspectors reviewed gaseous effluent summary data and the results of associated offsite dose calculations for selected dates between the fourth quarter of 2010 through the third quarter of 2011 to determine if indicator results were accurately reported.  The inspectors also reviewed the
licensee's methods for quantifying gaseous and liquid effluents and determining effluent dose.  Documents reviewed are listed in the Attachment
. Inspection Scope
 
45 Enclosure  This inspection constituted one Radiological Effluent TS/ODCM radiological effluent
occurrences sample as defined in IP 71151 05.
b. No findings were identified.
Findings 4OA2 Identification and Resolution of ProblemsCornerstones:  Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical Protection
  (71152) .1 a. Routine Review of Items Entered into the Corrective Action Program
As part of the various baseline
      
      
      
      
13 Attachment LIST OF ACRONYMS USED ADAMS Agencywide Document Access Management System AF Auxiliary Feedwater ALARA As-Low-As-Is-Reasonably-Achievable ANSI American National Standards Institute ASME American Society of Mechanical Engineers CAP Corrective Action Program CFR Code of Federal Regulations CLB Current Licensing Basis DAW Dry Active Waste DG Emergency Diesel Generator DOT Department of Transportation EAL Emergency Action Level ESF Engineered Safety Feature HELB High Energy Line Break HVAC Heating, Ventilation, and Air Conditioning IMC Inspection Manual Chapter IP Inspection Procedure IR Inspection Report IR Issue Report IST Inservice Testing LER Licensee Event Report LORT Licensed Operator Requalification Training MEER Miscellaneous Electrical Equipment Room MG Motor Generator NEI Nuclear Energy Institute OBE Operating Basis Earthquake ODCM Offsite Dose Calculation Manual OOS Out of Service OpEval Operability Evaluation OSP Outage Safety Plan OWA Operator Workaround psig pound per square inch gauge MSPI Mitigating Systems Performance Index NCV Non-Cited Violation NRC U.S. Nuclear Regulatory Commission NVLAP National Voluntary Laboratory Accreditation Program PI Performance Indicator RCS Reactor Coolant System RFO Refueling Outage RHR Residual Heat Removal RWST Refueling Water Storage Tank SDP Significance Determination Process SH Station Heating SRP Standard Review Plan SSC Structure, System, and Component SX Essential Service Water TLD Thermoluminescent Detector TS Technical Specification
13 Attachment
14 Attachment UFSAR Updated Final Safety Analysis Report UL Underwriters Laboratory URI Unresolved Item VA Auxiliary Building Ventilation WO Work Order
  LIST OF ACRONYMS USE
  M. Pacilio     -2-  In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). Sincerely,  /RA/  Eric R. Duncan, Chief Branch 3 Division of Reactor Projects Docket Nos. 50-454; 50-455 License Nos. NPF-37; NPF-66  Enclosure: Inspection Report No. 05000454/2011005 and 05000455/2011005    w/Attachment:  Supplemental Information cc w/encl: Distribution via ListServ                 DOCUMENT NAME:  G:\DRPIII\BYRO\Byron 2011 005.docx Publicly Available Non-Publicly Available Sensitive  Non-Sensitive To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy OFFICE RIII        NAME EDuncan:dtp   DATE 02/07/12    OFFICIAL RECORD COPY
D ADAMS Agencywide Document Access Management System
  Letter to M. Pacilio from E. Duncan dated February 7, 2012.   SUBJECT: BYRON STATION, UNITS 1 AND 2, NRC INTEGRATED INSPECTION REPORT 05000454/2011005; 05000455/2011005   
AF Auxiliary Feedwater
  DISTRIBUTION: Breeda Reilly RidsNrrDorlLpl3-2 Resource RidsNrrPMByron Resource  
ALARA As-Low-As-Is-Reasonably
RidsNrrDirsIrib Resource Cynthia Pederson  
-Achievable
Jennifer Uhle Steven Orth Jared Heck Allan Barker Carole Ariano Linda Linn DRPIII DRSIII Patricia Buckley Tammy Tomczak ROPreports.Resource@nrc.gov    
ANSI American National Standards Institute
 
ASME American Society of Mechanical Engineers CAP Corrective Action Program
CFR Code of Federal Regulations
CLB Current Licensing Basis
DAW Dry Active Waste
DG Emergency Diesel Generator
DOT Department of Transportation
EAL Emergency Action Level
ESF Engineered Safety Feature
HELB High Energy Line Break
HVAC Heating, Ventilation, and Air Conditioning
IMC Inspection Manual Chapter
IP Inspection Procedure
IR Inspection Report
IR Issue Report
IST Inservice Testing
LER Licensee Event Report
LORT Licensed Operator Requalification Training
MEE R Miscellaneous Electrical Equipment Room
MG Motor Generator
NEI Nuclear Energy Institute
OBE Operating Basis Earthquake
ODCM Offsite Dose Calculation Manual
OOS Out of Service
OpEval Operability Evaluation
OSP Outage Safety Plan
OWA Operator Workaround
ps ig pound per square inch gauge
MSPI Mitigating Systems Performance Index
NCV Non-Cited Violation
NRC U.S. Nuclear Regulatory Commission
NVLAP National Voluntary Laboratory Accreditation Program
PI Performance Indicator
RCS Reactor Coolant System
RFO Refueling Outage
RHR Residual Heat Removal
RWST Refueling Water Storage Tank
SDP Significance Determination Process
SH Station Heating
SRP Standard Review Plan
SSC Structure, System, and Component
SX Essential Service Water
TLD Thermoluminescent Detector
TS Technical Specification
 
14 Attachment
  UFSAR Updated Final Safety Analysis Report
UL Underwriters Laboratory
URI Unresolved Item
VA Auxiliary Building Ventilation
WO Work Order
 
  M. Pacilio
      -2-  In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document syste
m (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading
-rm/adams.html
(the Public Electronic Reading Room).
Sincerely,  /RA/  Eric R. Duncan, Chie f Branch 3 Division of Reactor Projects Docket Nos. 50
-454; 50-455 License Nos. NPF
-37; NPF-66  Enclosure:
Inspection Report No. 05000454/
2011005 and 05000455/
2011005    w/Attachment:  Supplemental Information
  cc w/encl:
Distribution via ListServ
                DOCUMENT NAME:   
G:\DRPIII\BYRO\Byron 2011 005.docx
  Publicly Available
  Non-Publicly Available
  Sensitive  Non-Sensitive To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy
OFFICE RIII        NAME EDuncan:dtp
    DATE 02/07/12    OFFICIAL RECORD COPY
 
  Letter to M. Pacilio from E. Duncan dated February 7, 2012.
  SUBJECT: BYRON STATION, UNITS
1 AND 2, NRC INTEGRATED INSPECTION REPORT 05000454/2011005; 05000455/2011005   
  DISTRIBUTION:
Breeda Reilly
RidsNrrDorlLpl3
-2 Resource
RidsNrrPMByron Resource
RidsNrrDirsIrib Resource
Cynthia Pederson
Jennifer Uhle
Steven Orth
Jared Heck
Allan Barker
Carole Ariano
Linda Linn
DRPIII DRSIII Patricia Buckley
Tammy Tomczak
ROPreports.Resource@nrc.gov
}}
}}

Revision as of 15:28, 30 July 2018

IR 05000454-11-005, IR 05000455-11-005; 10/01/2011 - 12/31/2011; Byron Station, Units 1 & 2; Operability Evaluations and Functional Assessments; Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and Transportati
ML12038A072
Person / Time
Site: Byron  Constellation icon.png
Issue date: 02/07/2012
From: Duncan E R
Region 3 Branch 3
To: Pacilio M J
Exelon Generation Co, Exelon Nuclear
References
IR-11-005
Download: ML12038A072 (69)


See also: IR 05000454/2011005

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION III

2443 WARRENVILLE ROAD, SUITE 210

LISLE, IL 60532

-4352 February 7, 2012

Mr. Michael J. Pacil

i o Senior Vice President, Exelon Generation Company, LLC

President and Chief Nuclear Office (CNO), Exelon Nuclear

4300 Warrenville Road

Warrenville, IL

60555 SUBJECT: BYRON STATION, UNITS

1 AND 2, NRC INTEGRATED INSPECTION REPORT 05000454/2011005; 05000455/2011005 Dear Mr. Pacilio

On December 31, 2011, the U.S. Nuclear Regulatory Commission (NRC) completed a

n integrated inspection

at your Byron Station, Units 1 and 2. The

enclosed inspection report documents the inspection findings which were discussed on

January 12, 2012

, with Mr. B. Youman and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

Three NRC-identified

findings of very low safety significance (Green) were identified

during this inspection. These findings were determined to involve violations of NRC requirements. Further, a licensee-identified violation which was determined to be of very low safety significance is listed in this report. The NRC is treating these violations as n

on-cited violations (NCVs) consistent with Section 2.3.2 of the NRC Enforcement Policy.

If you contest these

NCV s, you should provide a response

within 30 days of the date of this inspection report, with the basis for your denial, to

the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555

-0001, with a

copy to the Regional Administrator, U.S. Nuclear Regulatory Commission

- Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532

-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555

-0001; and the Resident Inspector Office at the Byron Station. If you disagree with a cross

-cutting aspect assignment

in this report, you should provide a response within 30 days of

the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region III, and the NRC Resident Inspector at the Byron Station.

M. Pacilio

-2- In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter , its enclosure, and your response (if any)

will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of

NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading

-rm/adams.html

(the Public Electronic Reading Room).

Sincerely, /RA/ Eric R. Duncan, Chie f Branch 3 Division of Reactor Projects Docket Nos. 50

-454; 50-455 License Nos. NPF

-37; NPF-66 Enclosure:

Inspection Report No. 05000454/

2011005 and 05000455/

2011005 w/Attachment: Supplemental Information

cc w/encl:

Distribution via ListServ

Enclosure U. S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket Nos:

50-454; 50-455 License Nos:

NPF-37; NPF-66 Report Nos:

05000454/2011005 and 05000455/

2011005 Licensee: Exelon Generation Company, LLC

Facility: Byron Station, Units 1 and 2

Location: Byron, IL Dates: October 1, 2011, through December

31, 2011 Inspectors:

B. Bartlett, Senior Resident Inspector

J. Robbins, Resident Inspector

R. Ng, Project Engineer

J. Dalzell

-Bishop, DRS Emergency Response Specialist

J. Cassidy, Senior Health Physicist

R. Jickling, Senior Emergency Preparedness Inspector

B. Palagi, Senior Operations Engineer

J. Nance, Reactor Engineer J. Benjamin, Braidwood Senior Resident Inspector

C. Thompson, Resident Inspector, Illinois Emergency

Management Agency

Approved by:

E. Duncan, Chief Branch 3 Division of Reactor Projects

Enclosure TABLE OF CONTENTS

REPORT DETAILS

................................................................................................

....................

4 Summary of Plant Status

................................................................................................

........ 4 1R01 Adverse Weather Protection (71111.01)

............................................................

4 1R04 Equipment Alignment (71111.04)

................................................................

...... 5 1R05 Fire Protection (71111.05)

................................................................

.................

6 1R11 Licensed Operator Requalification Program (71111.11)

................................

.... 7 1R12 Maintenance Effectiveness (71111.12)

..............................................................

8 1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

......... 9 1R15 Operability Evaluations (71111.15)

...................................................................10 1R19 Post-Maintenance Testing (71111.19)

................................

..............................

17 1R20 Outage Activities (71111.20)

............................................................................

18 2. REACTOR SAFETY

................................................................................................

...20 1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)

................

20 1EP6 Drill Evaluation (71114.06)

................................................................

...............

21 3. RADIATION SAFETY

................................................................................................

.21 2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01)

..............

21 2RS3 In-Plant Airborne Radioactivity Control and Mitigation (71124.03)

....................

24 2RS4 Occupational Dose Assessment (71124.04)

.....................................................

25 2RS5 Radiation Monitoring Instrumentation (71124.05)

................................

.............

26 2RS6 Radioactive Gaseous and Liquid Effluent Treatment (71124.06)

......................

26 2RS7 Radiological Environmental Monitoring Program (71124.07)

............................

32 2RS8 Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and Transportation (71124.08)

...........................................................................

34 4. OTHER ACTIVITIES

................................................................................................

...40 4OA1 Performance Indicator Verification (71151)

................................

.......................

40 4OA2 Identification and Resolution of Problems (71152)

................................

............

45 4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153)

...............

47 4OA6 Management Meetings

.....................................................................................

48 4OA7 Licensee-Identified Violations

...........................................................................

48 SUPPLEMENTAL INFORMATION

.............................................................................................

1 Key Points of Contact

................................................................

................................

.............

1 List of Items Opened, Closed, and Discussed

................................................................

........ 1 List Of Documents Reviewed

................................................................................................

.. 3 List Of Acronyms Used

................................................................................................

..........

13

1 Enclosure SUMMARY OF FINDINGS

Inspection Report (IR) 05000454/2011005, 05000455/2011005; 10/01/2011

- 12/31/2011;

Byron Station, Units 1 &

2; Operability Evaluations

and Functional Assessments; Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and Transportation

This report covers a

3-month period of inspection by resident inspectors and announced baseline inspections by regional inspector

s. Three Green findings were identified by the inspectors. The findings were considered Non-Cited Violation

s (NCVs) of NRC regulations. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP). Assigned cross-cutting aspects were determined using IMC

0310, "Components Within the Cross

-Cutting Areas." Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review.

The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG

-1649, "Reactor Oversight Process," Revision 4, dated December 2006.

A. Cornerstone: Mitigating Systems

NRC-Identified and Self

-Revealed Findings

Green. The inspectors identified a finding of very low safety significance and an associated NCV of 10 CFR Part 50, Appendix B, Criterion

XVI, "Corrective Action," when licensee personnel failed to identify voided piping between Unit 1 valves 1AF006B and 1AF017B and Unit 2 valves 2AF006B and 2AF 017B of the auxiliary feedwater (AF) system. The piping between these valves had been historically voided until they were recently re

-design ed to be filled and maintained filled with water to address a

n NRC-identified Green

finding and an associated NCV of 10 CFR Part 50, Appendix B, Criterion III, "Design Control

." The licensee entered this issue into their Corrective Action Program (CAP) as IR 1296819, IR 1292337, and IR 1295760. Corrective actions include d instituting

an Operations Standing Order, replacing the Unit 1 AF drain valve, and the isolation of the Unit 2 AF drain valve.

This finding was determined to be more than minor because it was associated with th

e Design Control attribute of the Mitigating Systems

Cornerstone

and adversely affected the cornerstone objective of ensuring the availability, reliability and capability of systems

that respond to initiating events to prevent undesirable consequences (i.e., core damage). The inspectors determined that the finding could be evaluated using the SDP in accordance with IMC 0609, "Significance Determination Process," Attachment

0609.04, "Phase 1

- Initial Screening and Characterization of Findings," Table 4a for the Mitigating

Systems Cornerstone.

Specifically, the inspectors answered "Y es" to Question 1

- Is the finding a design or qualification deficiency confirmed not to result in a loss of operability or functionality?

Based upon this Phase 1 screening, the inspectors concluded that the finding was of very low safety significance (Green). This finding had a cross-cutting aspect in t

he Resources component of the

Human Performance cross

-cutting area H.2(c) because the licensee did not have adequate procedures to ensure that piping between Unit 1 valves 1AF006B and 1AF017B and Unit 2 valves 2AF006B and 2AF017B were maintained filled with water. (Section 1R15)

2 Enclosure GreenThis finding was determined to be more than minor

because it was associated with the Design Control attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective of ensuring

the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). The inspectors determined that the finding could be evaluated using the SDP in accordance with IMC 0609, "Significance Determination Process," Attachment

0609.04, "Phase 1

- Initial Screening and Characterization of Findings," Table 4a, for the Mitigating Systems cornerstone. Specifically, the inspectors answered "No" to all of the Mitigating Systems Cornerstone questions in Table 4a.

Based upon this Phase 1 screening, the inspectors concluded that the finding was of very low safety significance (Green). This finding had

a cross-cutting aspect in the Corrective Action Program component of the Problem Identification and Resolution cross-cutting area P.1(c) because

the licensee failed to thoroughly evaluate the impact on operability of a

non-conforming condition associated with hazard barrier damper closure times. (Section 1R15) . The inspectors identified a finding of very low safety significance and an associated NCV of 10 CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," when licensee personnel failed to adhere to

Operability Determination Process standards after identifying a non

-conservative assumption related to closure times for hazard barrier dampers separating the Turbine Building from various safety

-related rooms within the Auxiliary Building. In particular, the issues raised by the inspectors during their review of Operability Evaluation 11-006, Revision 1, resulted in the station

re-evaluating the non

-conservative assumptions against aspects of the current licensing basis (CLB) not previously considered, and substantially revising the Operability Evaluation.

The licensee entered these issues into their CAP as IR 1184258, IR 1237133, IR 1238611, IR 1240295, IR 1244251, and IR

1276895. In addition to revising Operability Evaluation 2011

-006, corrective actions included an assignment

to reconstitute

design basis calculation records and plans to re

-design the hazard barrier dampers. Cornerstone: Public Radiation Safety

Green. A self-revealed finding of very low safety significance and an associated

NCV of 10 CFR 71.5, "Transportation of

Licensed Material," was identified when licensee personnel failed to comply with 49 CFR 172.203(c) and shipped packages of radioactive material with transport manifest

s that did not document all applicable hazardous substances. The issue

was entered in the licensee's CAP as IR 1285148.

Immediate corrective actions included providing

a corrected copy of the transport manifest to the waste processor. Further, the licensee placed locks on the shipping containers to control items placed in the packages and to ensure that the manifest accurately represented the hazards contained in the shipping packages.

This finding was determined to be more than minor because it was associated with the Program and Process attribute of the Public Radiation Safety

Cornerstone

a nd adversely affected the cornerstone objective

of ensuring adequate protection of public health and safety from exposure to radioactive materials released into the public domain as a result

of routine civilian nuclear reactor operation, in that, providing

incorrect information, as part of hazard

s communication

s, could impact the actions of response personnel. The inspectors determined that the finding could be evaluated using the SDP in accordance with IMC 0609, "Significance Determination Process," Appendix D, "Public Radiation

3 Enclosure Safety Significance Determination Process." Using the Public Radiation Safety SDP, the inspectors determined

(1) radiation limits were not exceeded; (2) there was no breach of a package during transit; (3) this issue

did not involve a certificate of compliance

(4) this issue was not a low level burial ground nonconformance; and (5) this issue

did not involve a failure to make notifications or provide emergency information.

As a result, the finding screened as having very low safety significance (Green). This finding had

a cross-cutting aspect in the Work Control component

of the Human Performance cross-cutting area H.3(b) since the licensee failed to coordinate work activities by incorporating actions to address the impact of

the work on different job activities, and the need for work groups to maintain interfaces with offsite organizations, and communicate, coordinate, and cooperate with each other during activities in which interdepartmental

coordination was necessary to assure adequate human performance

. Specifically, these events occurred because the licensee did not control the items

placed in the waste packages and was not present when the boxes were loaded.

(Section 2RS8)

B. One violation of very

low safety significance that was

identified by the licensee has been reviewed by the inspectors.

Corrective actions planned or taken by the licensee have been entered into the licensee's CAP. This violation and the associated corrective

action tracking number

are listed in Section 4OA7 of this report.

Lic ensee-Identified Violations

4 Enclosure REPORT DETAILS

Unit 1 operated at or near full power from the beginning of the inspection period until November 11, 2011, when power was reduced to 89 percent

to perform scheduled turbine throttle and governor valve testing. The unit was returned to full power the following day

and operated at full power for the remainder of the assessment period. Summary of Plant Status

Unit 2 began the inspection period shut down and in a planned refueling outage. The unit was restarted and returned to service on October 10, 2011. On November 5, 2011, reactor power was reduced to 96 percent to perform feedwater heater maintenance. The unit was returned to full power on November 14, 2011

, and operated at full power for the remainder of the inspection period. 1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity and Emergency Preparedness

1R01 Adverse Weather Protection

.1 (71111.01)

a. Winter Seasonal Readiness Preparations

The inspectors conducted a review of the licensee's preparations for winter conditions to verify that the plant's design features and implementation of procedures were sufficient to protect mitigating systems from the effects of adverse weather. Documentation for selected risk

-significant systems was reviewed to ensure that these systems would remain functional when challenged by inclement weather. During the inspection, the inspectors focused on plant specific design features and the licensee's procedures used to mitigate or respond to adverse weather conditions. Additionally, the inspectors reviewed the Updated Final Safety Analysis Report (UFSAR) and performance requirements for systems selected for inspection, and verified that operator actions were appropriate as specified by plant specific procedures. Cold weather protection, such as heat tracing and area heaters, was verified to be in operation where applicable.

The inspectors also reviewed Corrective Action Program (CAP) items to verify that the licensee was identifying adverse weather issues at an appropriate threshold and entering them into their CAP in accordance with station corrective action procedures. Specific documents reviewed during this inspection are listed in the Attachment. The

inspectors' reviews focused specifically on the following plant systems due to their risk significance or susceptibility to cold weather issues:

Inspection Scope

Station Heating System (SH);

Auxiliary Building Heating, Ventilation, and Air

-Conditioning (HVAC) [VA]; and Refueling Water Storage Tanks

(RWST s). This inspection constituted

one winter seasonal readiness

preparation

sample as defined in Inspection Procedure (IP) 71111.01-05.

5 Enclosure b. No findings were identified.

Findings 1R04 Equipment Alignment

.1 (71111.04)

a. Quarterly Partial System Walkdowns

The inspectors performed partial system walkdowns of the following risk

-significant systems: Inspection Scope

Unit 2 Train A Residual Heat Removal System Following Restoration to its Standby Line-U p; Unit 2 Train B Essential Service Water (SX) with the Unit 2 Train A SX Out-of-Service (OOS); Unit 2 Train B

Auxiliary Feedwater (AF) with the Unit 2 Train A AF OOS; and Unit 1 Train A AF with the Unit 1 Train B AF OOS

. The inspectors selected these systems

based on their risk significance relative to the

Reactor Safety Cornerstones at the time they were inspected. The inspectors attempted to identify any discrepancies that could impact the function of the system, and, therefore, potentially increase risk.

The inspectors reviewed applicable operating procedures, system diagrams, UFSAR, Technical Specification (TS) requirements, outstanding work

orders (WOs), condition reports, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have rendered the systems

incapable of performing their intended functions. The inspectors also walked down accessible portions of the systems to verify system components and support equipment were aligned correctly and operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no obvious deficiencies. The inspectors also verified that the licensee had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the CAP with the appropriate significance characterization. Documents reviewed are listed in the

Attachment. These activities constituted four partial system walkdown samples as defined in

IP 71111.04-05. b. No findings were identified.

Findings

6 Enclosure 1R05 Fire Protection

.1 (71111.05)

Routine Resident Inspector Tours

a. (71111.05Q)

The inspectors conducted fire protection walkdowns which were focused on availability, accessibility, and the condition of firefighting equipment in the following risk

-significant plant areas:

Inspection Scope

Unit 1 426

' Turbine Building (Fire Zone 8.5

-1); Unit 1 426

' Turbine Building (Fire Zone 8.5-1); Unit 1 Train B Auxiliary Feedwater Pump Room (Fire Zone 11.4A

-1); and Unit 2 Train B Auxiliary Feedwater Pump Room (Fire Zone 11.4A

-2 ). The inspectors reviewed areas to assess if the licensee had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant, effectively maintained fire detection and suppression capability, maintained passive fire protection features in good material condition, and implemented adequate compensatory measures for out

-of-service, degraded or inoperable fire protection equipment, systems, or features in accordance with the licensee's fire plan. The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plant's Individual Plant Examination of External Events with later additional insights, their potential to impact equipment which could initiate or mitigate a plant transient, or their impact on the plant's ability to respond to a security event. Using the documents listed in the Attachment, the inspectors verified that fire hoses and extinguishers were in their designated locations and available for immediate use; that

fire detectors and sprinklers were unobstructed;

that transient material loading was within the analyzed limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory condition. The inspectors also verified that minor issues identified during the inspection were entered into the licensee's CAP. Documents reviewed are listed in the Attachment

. These activities constituted four quarterly fire protection inspection samples as defined in

IP 71111.05-05. b. No findings were identified.

Findings .2 Annual Fire Protection Drill Observation

a. (71111.05A)

On November 11, 2011 , and December 17, 2011, the inspectors observed a fire brigade activation Fire Drill in the Unit 1 Auxiliary Boiler Room, 401' Elevation (Fire Zone 8.3

-1 SE). Based on this

observation, the inspectors

evaluated the readiness of the plant

fire brigade to fight fires. The inspectors verified that the licensee staff identified deficiencies; openly discussed them in a self

-critical manner at the drill debrief, and took appropriate corrective actions. Specific attributes evaluated were:

Inspection Scope

7 Enclosure proper wearing of turnout gear and self

-contained breathing apparatus;

proper use and layout of fire hoses;

employment of appropriate fire fighting techniques;

sufficient firefighting equipment brought to the scene;

effectiveness of fire brigade leader communications, command, and control;

search for victims and propagation of the fire into other plant areas;

smoke removal operations;

utilization of pre

-planned strategies;

adherence to the pre

-planned drill scenario; and

drill objectives.

Documents reviewed

are listed in the Attachment to this report.

These activities constituted one annual fire protection inspection sample as defined in

IP 71111.05-05. b. No findings were identified.

Findings 1R11 Licensed Operator Requalification Program

.1 (71111.11)

Annual Operating Test Results

a. (71111.11B)

The inspectors reviewed the overall pass/fail results of the Annual Operating Test,

administered by the licensee from October 18, 2011

through December 8, 2011, required by 10

CFR 55.59(a). The results were compared to the thresholds established in IMC 0609, Appendix I, "Licensed Operator Requalification Significance Determination Process (SDP)," to assess the overall adequacy of the licensee's Licensed Operator Requalification Program (LORT) to meet the requirements of

10 CFR 55.59. Inspection Scope

This inspection constitutes one biennial

and one annual

licensed operator requalification inspection sample as defined in IP

71111.11B and IP71111.11A

. b. No findings were identified.

Findings .2 Resident Inspector Quarterly Review

a. (71111.11Q)

On November 16, 2011, the inspectors observed a crew of licensed operators in the plant's simulator during licensed operator requalification examinations to verify that operator performance was adequate, evaluators were identifying and documenting crew performance problems and training was being conducted in accordance with licensee procedures. The inspectors evaluated the following areas:

Inspection Scope

8 Enclosure licensed operator performance;

crew's clarity and formality of communications;

ability to take timely actions in the conservative direction;

prioritization, interpretation, and verification of annunciator alarms;

correct use and implementation of abnormal and emergency procedures;

control board manipulations;

oversight and direction from supervisors; and

ability to identify and implement appropriate TS actions and

emergency plan actions and notifications.

The crew's performance in these areas was compared to pre

-established operator action expectations and successful critical task completion requirements.

Documents reviewed are listed in the Attachment.

In addition, the inspectors observed licensed operator performance in the actual plant and the main control room during this calendar quarter.

This inspection constituted one

quarterly licensed operator requalification program sample as defined in IP

71111.11. b. No findings were identified.

Findings 1R12 Maintenance Effectiveness

.1 (71111.12)

Routine Quarterly Evaluations

a. (71111.12Q)

The inspectors evaluated degraded performance

issues involving the following

risk-significant systems:

Inspection Scope

Unit 1 Rod Drive Motor Generator (MG) Set High Vibrations; and High Energy Line Break (HELB) Dampers.

The inspectors reviewed events

including those in which

ineffective equipmen

t maintenance had

resulted in valid or invalid automatic actuations of

engineered

safeguards

systems and independently verified the licensee's actions to address system performance or condition problems in terms of the following:

implementing appropriate work practices;

identifying and addressing common cause failures;

scoping of systems in accordance with

10 CFR 50.65(b) of the Maintenance Rule; characterizing system reliability issues for performance;

charging unavailability for performance;

trending key parameters for condition monitoring;

ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re

-classification; and

verifying appropriate performance criteria for structures, systems, and

components (SSCs)/functions classified as (a)(2) or appropriate and

adequate goals and corrective actions for systems classified as (a)(1).

9 Enclosure The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the system. In addition, the inspectors verified maintenance effectiveness issues were entered into the CAP with the appropriate significance characterization. Documents reviewed are listed in the

Attachment.

This inspection constituted two quarterly maintenance effectiveness sample as defined in IP 71111.12-05. b. No findings were identified.

Findings 1R13 Maintenance Risk Assessments and Emergent Work Control

.1 (71111.13)

a. Maintenance Risk Assessments and Emergent Work Control

The inspectors reviewed the licensee's evaluation and management of plant risk for the maintenance and emergent work activities affecting risk

-significant and safety

-related equipment listed below to verify that the appropriate risk assessments were performed prior to removing equipment for work:

Inspection Scope

Shutdown Safety Associated with Cavity Drain

Unit Common B Fire Pump OOS With SX as its Backup While O

ne Train of SX was OOS; Review of Planned Risk Significant Activities During Elevated Winds and Low River Level; and Unit 2 Train B Auxiliary Feedwater Pump OOS. These activities were selected based on their potential risk significance relative to the

Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that risk assessments were performed as required by

10 CFR 50.65(a)(4) and were accurate and complete. When emergent work was performed, the inspectors verified that the plant risk was promptly reassessed and managed. The inspectors reviewed the scope of maintenance work, discussed the results of the assessment with the licensee's

probabilistic risk analyst or shift technical advisor, and verified plant conditions were consistent with the risk assessment. The inspectors also reviewed TS requirements and walked down portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met.

These maintenance risk assessments and emergent work control activities constituted four samples as defined in IP

71111.13-05. b. No findings were identified.

Findings

10 Enclosure 1R15 Operability Evaluations

.1 (71111.15)

a. Operability Evaluations

The inspectors reviewed the following issues:

Inspection Scope

Unit 1 Embedment Plate 1SI06025V Due to Questions Regarding Supporting Analysis/Calculations

Unit 1 Seismic Support 1FW01147X Due to Questions Regarding Impact to HELB Analysis; Unit 1 and Unit 2 Train B AF

Pump s Due to Questions Regarding Multiple Starts

Unit 1 Leading Edge Flow Monitor Due to Identified Anomaly in Trended Data
Unit 1 and Unit 2 Train B A

F Pump s Due to Potential Pipe Voids in Cross

-Tie Piping; and Unit 1 Engineered Safety Features Switchgear Rooms Division 11 and 12 Due to Questions Regarding 1VX20Y and 1VX17Y Fire Damper "S" Hooks Preventing Closure of Dampers

The inspectors selected these potential operability issues based on the risk

significance of the associated components and systems. The inspectors evaluated the

technical adequacy of the evaluations to ensure that TS operability was properly justified and the

subject component or system remained available such that no unrecognized increase in

risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the

TS and U FSAR to the licensee's evaluations to determine whether the components or systems were operable. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. The inspectors determined, where appropriate, compliance with bounding limitations associated with the evaluations. Additionally, the inspectors reviewed a sample of corrective action documents to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations.

Documents reviewed are listed in the

Attachment.

This operability inspection constituted six

samples as defined in IP

71111.15-0 5. b. .1) Findings Failure to Identify Auxiliary Feedwater Pump Suction

Voids Introduction

The inspectors identified a finding of very low safety significance (Green)

and an associated NCV of 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," when licensee personnel failed to identify voided piping between Unit 1 valves 1AF006B and 1AF017B and Unit 2 valves

2AF006B and 2AF017B of the auxiliary feedwater system.

The piping between these valves had been historically voided until they were recently re

-design ed to be filled and maintained filled with water to address a

n NRC-identified Green finding and an associated NCV of 10 CFR Part 50, Appendix B, Criterion III, "Design Control"

(NCV 05000454/2011004

-04; 05000455/

-2011004-04, Design of Auxiliary Feedwater System Included Voids in Safety

-Related Alternate Suction Flow Paths)

.

11 Enclosure DescriptionOn November 17, 2011, the inspectors reviewed the Inspection Reports (I

Rs) generated

the previous day and

did not identify

any that documented the issue discussed above. The inspectors

re-inspected the tygon tubing between Unit 1 valves 1AF006B and 1AF017B and Unit 2 valves 2AF006B and

2AF017B and could not determine whether there was water in the tygon tubi ng. Licensee management was subsequently notified of the inspector's observations

. The licensee performed a system walkdown and confirmed that there was no visible wate r level in the tygon tubing

between Unit 1 valves 1AF006B and

1AF017B. The section of piping between the valves was subsequently filled with water and verified full through

ultrasonic testing.

On November

16, 2011, the inspectors notified licensee staff that there appeared to be no visible water in tygon tubing attached to vent valves between Unit 1 valves 1AF006B and

1AF017B and Unit 2 valves

2AF006B and

2AF017B. Visible water in tygon tubing attached to these vent valves was being used as an indication that the piping between these valves was filled with water. The inspectors could not determine whether there was water within the tygon tubing

because the inside of the tubing was

coated with a brown and

b lack substance suspected to be mold. The inspectors concluded that without

visible water in the tygon tubing , the space between these valves could be voided, contrary to plant design requirements. The piping between Unit 1 valves 1AF006B and 1AF017B and Unit 2 valves 2AF006B and 2AF017B

had been historically voided

, but were recently re

-designed and filled with water

to address a

n NRC-identifi ed Green finding and associated NCV of 10 CFR Part 50, Appendix B, Criterion III, "Design Control"

(NCV 05000454/2011004

-04; 05000455/

-2011004-04, Design of Auxiliary Feedwater System Included Voids in Safety

-Related Alternate Suction Flow Paths)

. The basis for this

Green finding and associated NCV was that the

licensee had not performed design reviews, calculations

, or suitable tests that demonstrated the voided piping between Unit 1 valves 1AF006B and 1AF017B and Unit 2 valves 2AF006B and 2AF017B would not adversely impact the ability of the AF system to perform its design function. This piping was downstream of the safety

-related essential service water (SX) supply for the diesel

-driven AF pumps

. The inspectors did observe standing water in the tygon tubing between Unit 1 valves 1AF006A and 1AF017A and Unit 2 valves 2AF006A and

2AF017A associated with the Unit 1 and Unit 2 motor-driven AF pumps

. On November 18, 2011, the inspectors

re-inspected the tygon tubing between Unit 1 valves 1AF006B and 1AF017B and Unit 2 valves 2AF006B and 2AF017B and could not determine whether there was water in the tygon tubing. The inspectors notified licensee management and questioned the licensee's actions to address the inspector's previous questions and concerns. The licensee performed a walkdown of the

system and confirmed the inspector's concern that the tygon tube was again empty , which indicated that the section of piping between Unit 1 valves AF006B and AF017B was likely voided. The licensee entered this issue into

their CAP. The section of piping

between the valves was again re-filled and verified full.

On November 29, 2011, the inspectors

performed field walkdowns and identified, again, that the tygon tubing attached to the vent line between Unit 2 valves 2AF006B and

2AF017 B did not have a visible water level. The inspectors notified licensee management and concluded

that the licensee did not have adequate measures in place to monitor or ensure the sections of piping between Unit 1 valves 1AF006B and

1AF017B and Unit 2 valves 2AF006B and 2AF017

B were maintained full of water.

The licensee performed a walkdown of the

system, confirmed the inspector's concerns, and

12 Enclosure filled the voided

section s of piping as before. In addition, the Operations

department instituted an Operations

Standing Order that required a

verification that the tygon tubing was filled with water multiple times a shift. The licensee entered this issue into

their CAP as IR 1296819, IR 1292337, and IR 1295760. Corrective actions incl

uded instituting the Operations Standing Order, replacing the Unit 1 AF drain valve, and isolating the Unit 2 AF drain valve.

AnalysisThis finding was determined to be more than minor because it was associated with th

e Design Control attribute of the Mitigating Systems

Cornerstone

and adversely affected the cornerstone objective of ensuring the availability, reliability and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). Specifically, the unverified configuration

might have rendered the Unit 1 and Unit 2 diesel

-driven AF pumps inoperable. : The inspectors determined that the failure to identify voided sections of AF piping prior to and following the inspector's observations and interactions with licensee management was a performance deficiency.

The inspectors determined that the finding could be evaluated using the SDP in accordance with IMC 0609, "Significance Determination Process," Attachment 0609.04, "Phase 1 - Initial Screening and Characterization of Findings," Table 4a for the Mitigating Systems Cornerstone.

Specifically, the inspectors answered

"Y es" to Question 1

- Is the finding a design or qualification deficiency confirmed not to result in a loss of operability or functionality?

This conclusion was reached after conservatively assuming that both sections of piping for Unit 1 and Unit 2 were completely voided and after reviewing tests performed by the licensee in response to the previously documented

design control Green finding and associated NCV

. These tests demonstrated that under the existing plant conditions, and even if the piping bet ween Unit 1 valves 1AF006B and 1AF017B and Unit 2 valves 2AF006B and 2AF017B was completely voided

, that the diesel-driven AF pumps were not inoperable. However, these tests were not of sufficient scope to demonstrate that under all possible plant conditions that the diesel

-driven AF pumps would have remained operable. Therefore

, although the existing void did not

render the diesel

-driven AF pumps inoperable

, there remained the possibility that under some conditions the unverified configuration discussed above

could have rendered the diesel-driven AF pumps inoperable.

Based upon this Phase 1 screening, the inspectors concluded that the finding was of very low safety significance (Green).

This finding

had a cross-cutting aspect in the

Resources component of the

Human Performance cross

-cutting area H.2(c) because the licensee did not ensure that procedures were adequate to ensure nuclear safety. In particular, licensee procedures did not ensure that the sections of piping between Unit 1 valves 1AF006B and 1AF017B

and Unit 2 valves 2AF006B and

2AF017B were maintained filled with water

as required

to support

nuclear safety

. EnforcementContrary to the above, licensee personnel failed to identify non

-conforming conditions associated with the station's safety

-related diesel

-driven AF systems. Spec

ifically, the

10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action

," requires, in part, that measures shall be established to assure that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment, and non

-conformances are promptly identified and corrected.

13 Enclosure space between Unit 1 valves 1AF006B and 1AF017B and Unit 2 valves 2AF006B and

2AF017B had been re

-designed to be full of water and was identified by the inspectors

prior to November 16, 2011; November 17, 2011;

November 18, 2011; and November 29, 2011 to be voided.

Corrective actions included filling the voided piping sections, replacing the Unit 1 drain valve, isolating the Unit 2 drain valve, and monitoring tygon tubing water

level on a more frequent basis. Because this violation was of very low safety significance and was entered into the licensee's CAP

as IR 1296819, IR 1292337, and IR 1295760, this violation is being treated as a NCV consistent with Section 2.3.2 of the NRC Enforcement Policy. (NCV 05000454/2011005

-01; 05000455/2011

005-01, Failure to Identify Voided Sections of AF Piping)

.2) Operability Evaluation Not Performed in Accordance with Station Standards

Introduction: The inspectors identified a finding of very low safety significance (Green) and an associated NCV of 10 CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," when licensee personnel failed to adhere to numerous

Operability Determination Process standards after identifying a non

-conservative

assumption related to closure times for hazard barrier dampers separating the Turbine

Building from various safety

-related rooms within the Auxiliary Building.

DescriptionThe inspectors reviewed Operability Evaluation 11

-006, Revision 1, and identified a number of exampl es in which the evaluation did not meet the standards

in OP-AA-108-115. Specifically, OP-AA-108-115, "Operability Evaluation Standard," Revision 9 included the following requirements:

On July 6, 2011, the licensee identified non

-conservative assumptions in the actuation time for fusible links used in hazard barrier dampers for the Engineered Safety Feature (ESF) Rooms, Non-ESF Switchgear

Rooms, Miscellaneous Electrical Equipment Rooms (MEERs) and Emergency Diesel Generator (DG) Rooms. These

dampers protected these rooms from the effects of a Turbine Building fire or HELB event. The applicable calculations of record assumed that these dampers shut within about 5 seconds of reaching a temperature of 165 degrees fahrenheit (°F). These dampers utilized a fusible link which was required to meet Underwriters Laboratories (UL) specifications (Heat Responsive Links for Fire Protection Service: UL 33). This specification

provided a formula for calculating an acceptable fusible link response time

as a function of temperature.

Using the UL formula, licensee personnel calculated that the expected thermal link response times were up to 100 seconds for the ESF

Switchgear Room dampers and 200 seconds for the MEER and Non

-ESF Switchgear dampers based on projected HELB temperature

s outside of these rooms. Therefore, the station calculations of record

assumed that these dampers would isolate the affected rooms from

a Turbine Building HELB much sooner than UL specifications. The licensee evaluated this non

-conservative condition in Operability

Evaluation 11

-006, Revision 1, concluded that there was reasonable assurance that the equipment affected in the

identified rooms would remain operable during a licensing basis HELB event. This conclusion was reached after the licensee had complete

d and approved Operability Evaluation 11-006 in accordance with OP

-AA-108-115, "Operability Evaluation Standard," Revision 9.

14 Enclosure OP-AA-108-115, Operability Evaluation Standard, Revision 9

The OpEval [Operability Evaluation] should contain sufficient detail for a knowledgeable individual to independently reach the same conclusions as the Preparer (i.e., the OpEval must be able to stand alone).

Section 4.4.2 1. The Preparer should examine the CLB [Current Licensing Basis] requirements or commitments, including the TSs and UFSA

R, to establish the conditions and performance requirements to be met for determining operability, as necessary. The scope of an OpEval needs to be sufficient to address the capability of the SSC to perform its specified safety functions.

The OpEval should address the following, as applicable . . . Determine the extent of condition for all similarly affected SSCs

. The inspectors identified the following examples that did not meet this standard:

Operability Evaluation 11

-006, Revision 1, did not evaluate the non

-conforming condition against the CLB single failure criterion.

This single failure criterion wa

s discussed in NRC Standard Review Plan (SRP) Section 3.6.1, Branch Technica

l Position (BTP) ASB 3-1, Section B.3.b(2). Branch Technical Position

ASB 3-1, Section B.3.b(2)

discussed how a single active component failure should be assumed in systems used to mitigate the consequences of a

postulated piping failure to shut down the reactor. After the inspectors discussed this requirement with the licensee, licensee personnel determined that the dampers needed to be considered for single failure during a HELB event. This CLB single failure criterion was readily available when the licensee examined the CLB requirements for this issue during the development of Operability Evaluation

11-006. The licensee entered this issue

into their CAP as IR 1244251.

Operability Evaluation 11

-006, Revision 1, did not adequately consider a pipe crack in accordance with the CLB. The CLB requirements for a pipe crack included a n assumed lower allowable stress threshold than for a broken or severed pipe. Specifically, Operability Evaluation 11

-006, Revision 1, did not address leakage cracks in accordance with Section III of the American Society of Mechanical Engineers (ASME) Code for Class 2 and Class 3 piping as referenced in Section

3.6.2.1.2.1.1, "Fluid System Piping Not in the Containmen

t Penetration Area," of the UFSAR. In particular, Section d of Section 3.6.2.1.2.1.1 stated, in part, "[L]eakage cracks in high energy ASME Section III Class 2 and 3 piping and seismically analyzed and supported ANSI [American Nuclear Standards Institute] B31.1 piping are postulated at locations where the stresses under the loadings resulting from normal and upset plant conditions and an OBE [Operating Basis Earthquake] event as calculated by equations (9) and (10) in Paragraph NC

-3652 of ASME Section III exceed 0.4 (1.2

multiplied times

Sh + Sa). The licensee entered this issue

into their CAP as IR 1240295.

Operability Evaluation 11

-006, Revision 1, did not address the extent of condition review for all similarly affected SSCs. The

inspectors identified a number of safety-related rooms that utilized the

same (or similar) style damper s in which the

15 Enclosure non-conforming condition applied

that were not evaluated. Those rooms included the

Unit 1 and Unit 2 Lower Cable Spreading R

oom Non-Segregated Bus Duct areas;

an electrical cable chase located above the

"B" Emergency Diesel Generator;

the station Emergency Diesel Ge

nerator Diesel Oil Storage Tank Rooms; and the Control Room Ventilation Makeup System , which could be aligned to take makeup air from the Turbine B

uilding. The licensee entered this issue into their CAP as IR 1279759 and IR 12776277.

Operability Evaluation 11

-006 , Revision 1, as associated with

MEER 12 and MEER 22 , did not identify a potential common mode failure after the inspectors determined

that the licensee had not adequately considered single failure. These rooms contain

ed both trains of Unit 1 and Unit 2 reactor trip and reactor trip bypass breakers

, respectively.

The event of concern was a Turbine Building HELB combined with the failure of either the MEER 12 or MEER 22 hazard barrier dampers to shut

, which would expose both trains of reactor trip breakers to a harsh steam environment. This equipment was not environmentally qualified

in accordance with 10 CFR 50.49. The licensee entered this issue

into their CAP as IR 1276895

. The inspectors were not able to reach the same conclusions as the Preparer when reviewing Operability Evaluation 11

-006, Revision 1, since Operability Evaluation 11

-006, Revision 1, lacked the necessary detail regarding assumptions and limitations

for the inspectors to

determine if the evaluation was consistent with station design. The

inspectors concluded that Operability Evaluation 11

-006, Revision 1, did not meet the licensee's

"stand alone" requirement

in OP-A A-108-115. On November 17, 2011, the licensee completed a substantial revision to Operability

Evaluation 11

-006, Revision 1, that addressed the issues previously identified

by the inspectors.

In addition to the issues described above, the inspectors identified that the station's applicable HELB calculations of records

had not considered the licensing

basis single failure. The inspectors determined that this historic issue contributed to the licensee's misunderstanding of the

ir CLB. The licensee entered these issues into the their CAP as IR 1184258, IR 1237133, IR 1238611, IR 1240295, IR 1244251, and IR

1276895. Corrective actions include two revisions of Operability Evaluation 11

-006, an assignment to reconstitute the applicable design basis calculation records, and plans to re

-design the hazard barrier dampers

to provide additional margin.

AnalysisThis performance deficiency

was determined to be more than minor

because it was similar to the "not minor if" aspect of Example 3j in IMC 0612, Appendix E, "Example of Minor Issues

," since the errors in Operability Evaluation 11

-006, Revision 1, resulted in a condition in which there was a reasonable doubt on the operability of the systems and : The inspectors determined that the failure to meet the station Operability Determination process standards outlined in OP

-AA-108-115, "Operability Evaluation Standard," Revision 9, during the evaluation of a non

-conforming condition was a performance deficiency.

16 Enclosure components that were the subject of the evaluation

an d dissimilar from the "minor

because" aspect of this example since the impact of the errors on Operability Determination 11

-006, Revision 1, was not minimal. In addition, the performance deficiency was determined to be more than minor because it was associated with the Design Control attribute of the Mitigating Systems

Cornerstone and adversely affected the cornerstone objective of ensuring

the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). The inspectors determined that the finding could be evaluated using the SDP in accordance with IMC 0609, "Significance Determination Process," Attachment 0609.04, "Phase 1 - Initial Screening and Characterization of Findings," Table 4a, for the Mitigating Systems

Cornerstone. Specifically, the inspectors answered

"No" to all of the Mitigating Systems Cornerstone questions in Table 4a.

As a result, the finding screened as having very low safety significance (Green).

This finding has a cross

-cutting aspect in the CAP component of the Problem Identification and Resolution cross

-cutting area P.1(c) since the licensee failed to thoroughly evaluate the impact on operability of a non-conforming condition associated with hazard barrier closure times.

EnforcementContrary to the above, the inspectors identified examples during the development of Operability Evaluation 11

-006, Revision 1, in which licensee personnel failed to adhere to quality procedure OP

-AA-108-115, "Operability Determinations (CM

-1)," Revision 9.

10 CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," require

s, in part, that activities affecting

quality shall be prescribed

by documented instructions, procedures, or drawings, of a type appropriate to the circumstance and shall be accomplished in accordance with these instructions,

procedures of drawings.

In particular, OP

-AA-108-115, Revision 9, stated in part:

"The OpEval should contain sufficient detail for a knowledgeable individual to independently reach the same conclusions as the Preparer (i.e., the OpEval must

be able to stand alone).

The Preparer should examine the CLB [Current Licensing Basis] requirements or commitments, including the TSs and UFSAR, to establish the conditions and performance requirements to be met for determining operability, as necessary. The scope of an OpEval needs to be sufficient to address the capability of the SSC

to perform its specified safety functions.

The OpEval should address the following, as applicable . . . Determine the extent of condition for all similarly affected SSCs

." Contrary to this requirement:

On July 15, 2011, the licensee did not adequately examine the applicable CLB requirements or commitments to establish the performance requirements to be met

17 Enclosure for determining operability in the case of single failure, common mode, and leakage crack assumptio

ns. On July 15, 2011, the licensee's "OpEval" did not adequately address the extent of condition for all similarly affected SSC

s. On July 15, 2011, the "OpEval" did not contain sufficient detail for a knowledgeable individual to independently reach the same conclusions as the Preparer. Because this violation was of very low safety significance and it was entered into the licensee's corrective actions program, this violation is being treated as a

NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy. (NCV 05000454/2011005

-02; 05000455/20110 05-02, Operability Evaluation Not Performed in Accordance with Station Standards)

1R19 Post-Maintenance Testing

.1 (71111.19)

a. Post-Maintenance Testing

The inspectors reviewed the following post

maintenance testing activities to verify

that procedures and test activities were adequate to ensure system operability and functional capability:

Inspection Scope

Unit 2 AF Check Valves

2AF014E, 2AF014G, and 2AF014H Following Disassembly and Inspection

Unit 2 Reactor Coolant Pump Motor

- 2D Following Refuel Maintenance and Inspection

Unit 2 Charging Valve Stroke Time and Position Indication Test 2CV8804A

F ollowing Circuit Modification

Unit 2 Solid State Protection System F

ollowing Unit 2 Refueling Outage Preventive Maintenance

Unit 2 Train B Containment Spra

y Following Replacement of Timer Relay

Unit 1 Train A Rod Drive Motor

-Generator Following Bearing Replacement; and Surveillance 2BOSR 0.5

-2.RH.4-1 Following Maintenance on Valve 2RH610

These activities were selected based upon the structure, system, or component's ability to impact risk. The inspectors evaluated these activities for the following (as applicable): the effect of testing on the plant had been adequately addressed; testing was adequate for the maintenance performed; acceptance criteria were

clear and demonstrated operational readiness; test instrumentation was appropriate; tests were performed as written in accordance with properly reviewed and approved procedures; equipment was returned to its operational status following testing (temporary

modifications or jumpers required for test performance were properly

removed after test completion);

and test documentation was properly evaluated. The inspectors evaluated the activities against

TS s, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various

NRC generic communications to ensure that the test results adequately ensured that the equipment met the licensing basis and design requirements. In addition, the inspectors reviewed corrective action documents associated with post

maintenance tests to determine whether the licensee was identifying problems and entering them in the CAP

18 Enclosure and that the problems were being corrected commensurate with their importance to safety. Documents reviewed are listed in the

Attachment.

This inspection constituted seven post maintenance testing samples as defined in

IP 71111.19-05. a. No findings were identified.

Findings 1R20 Outage Activities

.1 (71111.20)

a. Refueling Outage Activities

The inspectors reviewed the Outage Safety Plan (OSP) and contingency plans for the Unit 2 refueling outage (RFO) B2R16, conducted September 18 through October 10, 2011, to confirm that the licensee had appropriately considered risk, industry experience, and previous site

-specific problems in developing and implementing a plan that assured maintenance of defense

-in-depth. During the RFO, the inspectors observed portions of the shutdown and cooldown processes and monitored licensee controls over the outage

activities listed below. Documents reviewed during the inspection are listed in the Attachment to this report.

Inspection Scope

Licensee configuration management, including maintenance of defense

-in-depth commensurate with the OSP for key safety functions and compliance with the applicable TS when taking equipment out of service.

Implementation

of clearance activities and confirmation that tags were properly hung and equipment appropriately configured to safely support the work or

testing. Installation and configuration of reactor coolant pressure, level, and temperature instruments to provide accurate indication, accounting for instrument error.

Controls over the status and configuration of electrical systems to ensure that

TS and OSP requirements were met, and controls over switchyard activities.

Monitoring of decay heat removal processes, systems, and components.

Controls to ensure that outage work was not impacting the ability of the operators to operate the spent fuel pool cooling system.

Reactor water inventory controls

including flow paths, configurations, and alternative means for inventory addition, and controls to prevent inventory loss.

Controls over activities that could affect reactivity.

Maintenance of secondary containment as required by TS.

Licensee fatigue management, as required by 10 CFR 26, Subpart I.

Refueling activities, including fuel handling and sipping to detect fuel assembly

leakage. Startup and ascension to full power operation, tracking of startup prerequisites, walkdown of the drywell (primary containment) to verify that debris had not been left which could block emergency core cooling system suction strainers, and reactor physics testing.

Licensee identification and resolution of problems related to RFO activities.

19 Enclosure This inspection constituted one RFO sample as defined in IP

71111.20-05. b. No findings

were identified.

Findings 1R22 Surveillance Testing

.1 (71111.22)

a. Surveillance Testing

The inspectors reviewed the test results for the following activities to determine whether risk significant systems and equipment were capable of performing their intended safety function and to verify testing was conducted in accordance with applicable procedural

and TS requirements:

Inspection Scope

Unit 2 Train B

Diesel Generator Sequence Test;

Unit 1 Train B AF

Pump ASME Surveillance

Unit 1 Train B AF

Valve Strokes for 1AF013E

-H; Unit 1 Train B Residual Heat Removal (RHR) Check Valve 1SI8958B

Unit 2 Reactor Coolant System (RCS) Water Inventory Balance Surveillance (Leak Detection); and 0BMSR FP-5, Fire Hydrant Yard Loop Annual Flush

The inspectors observed

in-plant activities and reviewed procedures and associated records to determine the following:

did preconditioning occur

were the effects of the testing adequately addressed by control room personnel or

engineers prior to the commencement of the testing;

were acceptance criteria clearly stated, demonstrated operational readiness, and consistent with the system design basis;

plant equipment calibration was correct, accurate, and properly documented;

as left setpoints were within required ranges; and the calibration frequency were in accordance with TSs, the USAR, procedures, and applicable commitments;

measuring and test equipment calibration was current;

test equipment was used within the required range and accuracy; applicable prerequisites described in the test procedures were satisfied;

test frequencies met TS requirements to demonstrate operability and reliability; tests were performed in accordance with the test procedures and other applicable procedures; jumpers and lifted leads were controlled and restored where used;

test data and results were accurate, complete, within limits, and valid;

test equipment was removed after testing;

where applicable for inservice testing (IST) activities, testing was performed in accordance with the applicable version of Section

XI of the ASME

code, and reference values were consistent with the system design basis;

where applicable, test results not meeting acceptance criteria were addressed with an adequate operability evaluation or the system or component was declared inoperable;

20 Enclosure where applicable for safety

-related instrument control surveillance tests, reference setting data were accurately incorporated in the test procedure;

where applicable, actual conditions encountering high resistance electrical contacts were such that the intended safety function could still be accomplished;

prior procedure changes had not provided an opportunity to identify problems encountered during the performance of the surveillance or calibration test; equipment was returned to a position or status required to support the

performance of its safety functions;

and all problems identified during the testing were appropriately documented and dispositioned in the CAP.

Documents reviewed are listed

in the Attachment.

This inspection constituted four routine surveillance testing samples, one IST sample, and one RCS Leak

Detection sample, as defined in IP

71111.22, Sections

-02 and -05. b. No findings were identified.

Findings 2. REACTOR SAFETY

Cornerstone:

Emergency Preparedness

1EP4 Emergency Action Level and Emergency Plan Changes

.1 (71114.04)

a. Emergency Action Level and Emergency Plan Changes

Since the last NRC inspection of this program area, Emergency Action Levels (EALs) and Emergency Plan Revisions 27 and 28 were implemented based on the licensee's

determination, in accordance with 10

CFR 50.54(q), that the changes resulted in no decrease in effectiveness of the Plan, and that the revised Plan as changed continued

to meet the requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR Part 50. The inspectors conducted a sampling review of the Emergency Plan changes and a review of the EAL changes to evaluate for potential decreases in effectiveness of the Plan. However, these reviews do not constitute formal NRC approval of the changes. Therefore, these changes remain subject to future NRC inspection in their entirety.

Inspection Scope

This EAL and Emergency Plan changes inspection constituted one sample as defined in

IP 71114.04-05. b. No findings

were identified.

Findings

21 Enclosure 1EP6 Drill Evaluation

.1 (71114.06)

a. Emergency Preparedness Drill Observation

The inspectors evaluated the conduct of a routine licensee emergency drill on November 15, 2011, to identify any weaknesses and deficiencies in classification, notification, and protective action recommendation development activities. The inspectors observed emergency response operations in the Simulator Control Room

and Technical Support Center

to determine whether the

event classification, notifications, and protective action recommendations were performed in accordance with procedures. The inspectors also attended the licensee drill critique to compare

any inspector-observed weakness with those identified by the licensee staff in order

to evaluate the critique and

to verify whether the licensee staff was properly identifying weaknesses and entering them into the CAP. As part of the inspection, the inspectors reviewed the drill package and other documents listed in the Attachment

. Inspection Scope

This emergency preparedness drill

inspection constituted one sample as defined in

IP 71114.06-05. b. No findings were identified

. Findings 3. RADIATION SAFETY 2RS1 Radiological Hazard Assessment and Exposure ControlsThe inspection activities supplement those documented in Inspection Report 05000454/2011002; 05000455/2011002 and constitute one complete sample as defined in IP 71124.01

-05. (71124.01)

.1 Inspection Planning

a. (02.01) The inspectors reviewed licensee performance indicators for the occupational exposure cornerstone for follow

-up. The inspectors reviewed the results of radiation protection program audits (e.g., licensee

quality assurance audits or other independent audits). The inspectors reviewed reports

of operational occurrences related to occupational radiation safety since the last inspection. The inspectors reviewed the results of the audit and operational report reviews to gain insights into overall licensee performance.

Inspection Scope

b. No findings were identified.

Findings

22 Enclosure .2 Instructions to Workers

a. (02.03) The inspectors reviewed selected occurrences where a worker's electronic personal dosimeter noticeably malfunctioned or alarmed. The inspectors evaluated whether workers responded appropriately to the off-normal condition. The inspectors assessed whether the issue was included in the CAP and dose evaluations were conducted as appropriate.

Inspection Scope

b. No findings were identified.

Findings .3 Radiological Hazards Control and Work Coverage

a. (02.05) The inspectors examined the licensee's physical and programmatic controls for highly activated or contaminated materials (nonfuel) stored within spent fuel and other storage pools. The inspectors assessed whether appropriate controls (i.e., administrativ

e and physical controls) were in place to preclude inadvertent removal of these materials from

the pool.

Inspection Scope

The inspectors examined the posting and physical controls for selected high radiation areas and very

high radiation areas to verify conformance with the occupational radiation performance indicator.

b. No findings were identified.

Findings .4 Risk-Significant High Radiation Area and Very

High Radiation Area Controls

a. (02.06) The inspectors discussed with the radiation protection manager the controls and procedures for high

-risk high radiation areas and very

high radiation areas. The inspectors discussed methods employed by the licensee to provide stricter control of

very high radiation area access as specified in 10 CFR 20.1602, "Control of Access to Very High Radiation Areas," and Regulatory Guide 8.38, "Control of Access to High and Very High Radiation Areas of Nuclear Plants." The inspectors assessed whether any changes to licensee procedures

substantially reduce

d the effectiveness and level of worker protection.

Inspection Scope

The inspectors discussed the controls in place for special areas that have the potential to become very

high radiation areas during certain plant operations with health physics supervisors (or equivalent positions having backshift health physics oversight authority). The inspectors assessed whether these plant operations require

d communication beforehand with the health physics group, so as to allow corresponding timely actions to

23 Enclosure properly post, control, and monitor the radiation hazards including re

-access authorization.

The inspectors evaluated licensee controls for very

high radiation areas and areas with the potential to become very

high radiation areas to ensure that an individual was not able to gain unauthorized access to the very

high radiation area.

b. No findings were identified.

Findings .5 Radiation Worker Performance

a. (02.07) The inspectors reviewed radiological problem reports since the last inspection that found the cause of the event to be human performance errors. The inspectors evaluated whether there was an observable pattern traceable to a similar cause. The inspectors assessed whether this perspective matched the corrective action approach taken

by the licensee to resolve the reported problems. The inspectors discussed with the radiation

protection manager any problems with the corrective actions planned or taken.

Inspection Scope

b. No findings were identified.

Findings .6 Radiation Protection Technician Proficiency

a. (02.08) The inspectors reviewed radiological problem reports since the last inspection that found the cause of the event to be radiation protection technician error. The inspectors evaluated whether there was an observable pattern traceable to a similar cause. The inspectors assessed whether this perspective matched the corrective action approach taken by the licensee to resolve the reported problems.

Inspection Scope

b. No findings were identified.

Findings .7 Problem Identification and Resolution

a. (02.09) The inspectors evaluated whether problems associated with radiation monitoring and exposure control were being identified by the licensee at an appropriate threshold and were properly addressed for resolution in the licensee's CAP. The inspectors assessed the appropriateness of the corrective actions for a selected sample of problems

documented by the licensee that involve

d radiation monitoring and exposure controls. The inspectors assessed the licensee's process for applying operating experience to their plant.

Inspection Scope

24 Enclosure b. No findings were identified.

Findings 2RS3 In-Plant Airborne Radioactivity Control and MitigationThe inspection activities supplement those documented in Inspection Report 05000454/2011002; 05000455/2011002 and

constitute o

ne complete sample as defined in IP 71124.03

-05. (71124.03)

.1 Engineering Controls

a. (02.02) The inspectors reviewed the licensee's use of permanent and temporary ventilation to determine whether the licensee used

ventilation systems as part of its engineering controls (in

-lieu of respiratory protection devices) to control airborne radioactivity.

The inspectors reviewed procedural guidance for use of installed plant systems, such as

containment purge, spent fuel pool ventilation, and auxiliary building ventilation, an

d assessed whether the systems were used, to the extent practicable, during high

-risk activities (e.g., using containment purge during cavity flood

-up). Inspection Scope

The inspectors selected installed ventilation systems used to mitigate the potential for airborne radioactivity, and evaluated whether the ventilation airflow capacity, flow path (including the alignment of the suction and discharges), and filter/charcoal unit

efficiencies, as appropriate, were consistent with maintaining concentrations of airborne radioactivity in work areas below the concentrations of an airborne area to the extent

practicable.

The inspectors selected temporary ventilation system setups (high efficiency particulate air/charcoal negative pressure units, down draft tables, tents, metal "Kelly buildings," and other enclosures) used to support work in contaminated areas.

The inspectors assessed whether the use of these systems was consistent with licensee procedural

guidance and the As-Low-As-Reasonably

-Achievable (ALARA)

concept. The inspectors reviewed airborne monitoring protocols by selecting installed systems used to monitor and warn of changing airborne concentrations in the plant and evaluating whether the alarms

and setpoints were sufficient to prompt licensee/worker action to ensure that doses were maintained within the limits of 10 CFR Part 20 and the

ALARA concep t. The inspectors assessed whether the licensee had established trigger points (e.g., the

Electric Power Research Institute's "Alpha Monitoring Guidelines for Operating Nuclear Power Stations") for evaluating levels of airborne beta

-emitting (e.g., plutoni

um-241) and alpha-emitting radionuclides.

b. No findings were identified.

Findings

25 Enclosure .2 Use of Respiratory Protection Devices

a. (02.03) For those situations where it was impractical to employ engineering controls to minimize airborne radioactivity, the inspectors assessed whether the licensee provided respiratory protective devices such that occupational doses were ALARA. The inspectors selected work activities where respiratory protection devices were used to limit the intake of radioactive materials, and assessed whether the licensee performed an evaluation concluding that further engineering controls were not practical and that the use of respirators wa

s ALARA. The inspectors also evaluated whether the licensee had established means (such as routine bioassay) to determine if the level of protection (protection factor) provided by the respiratory protection devices during use was at least

as good as that assumed in the licensee's work controls and dose assessment.

Inspection Scope

b. No findings were identifi

ed. Findings 2RS4 Occupational Dose AssessmentThe inspection activities supplement those documented in Inspection Report 05000454/2011002; 05000455/2011002 and constitute one complete sample as defined in IP 71124.04

-05. (71124.04)

.1 External Dosimetry

a. (02.02) The inspectors evaluated whether the licensee's dosimetry vendor was National Voluntary Laboratory Accreditation Program (NVLAP) accredited and if the approved irradiation test categories for each type of personnel dosimeter used were consisten

t with the types and energies of the radiation present and the way the dosimeter wa

s

being used (e.g., to measure deep dose equivalent, shallow dose equivalent, or lens dose equivalent).

Inspection Scope

b. Findings Introduction

The inspectors identified that the licensee's use of dosimeters (TLDs) may not be consistent with the methods used by the NVLAP accreditation

process. As a result, the inspectors identified an Unresolved Item (URI) for the apparent

non-compliance with 10 CFR 20.1501(c)(2) because the accreditation process for the types of radiation included in the NVLAP program may not approximate the types of radiation for which the individual wearing the dosimeter is monitored.

Discussion

The licensee used

a vendor to supply and process dosimeters used to measure radiation exposure for the monitored workers.

This vendor was NVLAP accredited for beta, gamma, neutron, mixture of beta/gamma, and mixture neutron/gamma radiations. However, the licensee used

the dosimeters when workers may be exposed to beta, gamma, and neutron radiations within the same monitoring

26 Enclosure period. The inspectors determined that this mixture of three radiation types may not be aligned with the accreditation process.

The issue was categorized as a URI pending NRC evaluation of this practice and determination whether a single TLD can accurately measure occupational dose to three types of radiation (URI 05000454/2011005

-03; 05000455/2011005

-03; Use of TLDs May Not be Consistent with the Methods Used by the NVLAP Accreditation Process) 2RS5 Radiation Monitoring InstrumentationThe inspection activities supplement those documented in Inspection Report 05000454/2011002; 05000455/2011002 and constitute one complete sample as defined in IP 71124.05

-05. (71124.05)

.1 Inspection Planning

a. (02.01) The inspectors reviewed the area radiation monitor alarm setpoint values and setpoint bases as provided in the TSs and the Final Safety Analysis Report.

Inspection Scope

The inspectors reviewed effluent monitor alarm setpoint bases and the calculation methods provided in the Offsite Dose Calculation Manual (ODCM). b. No findings were identified.

Findings 2RS6 Radioactive Gaseous and Liquid Effluent TreatmentThis inspection constituted one complete sample as defined in IP 71124.06

-05. (71124.06)

.1 Inspection Planning and Program Reviews

(02.01) a. Event Report and Effluent Report Reviews

The inspectors reviewed the radiological effluent release reports issued since the last

inspection to determine if the reports were submitted as required by the ODCMl/TSs.

The inspectors reviewed anomalous results, unexpected trends, or abnormal releases identified by the licensee for further inspection to determine if they were evaluated, were entered in the CAP, and were adequately resolved.

Inspection Scope

The inspectors identified radioactive effluent monitor operability issues reported by the licensee in effluent release reports and review ed these issues during the onsite inspection, as warranted, and determine

d if the issues were entered into the CAP and adequately resolved

. b. No findings were identified.

Findings

27 Enclosure c. Offsite Dose Calculation Manual and Final Safety Analysis Report Review

The inspectors reviewed Final Safety Analysis Report descriptions of the radioactive effluent monitoring systems, treatment systems, and effluent flow paths so they could be evaluated during inspection walkdowns.

Inspection Scope

The inspectors reviewed changes to the ODCM made by the licensee since the last

inspection against the guidance in NUREG

-1301, NUREG-0133, and Regulatory Guides 1.109, 1.21 and 4.1. When differences were identified, the inspectors reviewed the technical basis or evaluations of the change during the onsite inspection to determine whether they were technically justified and maintain effluent releases ALARA. The inspectors

reviewed licensee documentation to determine if the licensee had

identified any n

on-radioactive systems that had

become contaminated as disclosed either through an event report or the ODCM since the last inspection. This review provided an intelligent sample list for the onsite inspection of any 10 CFR 50.59 evaluations and allowed a determination if any

newly contaminated systems had

an unmonitored effluent discharge path to the environment, whether any required OD

C M revisions were made to incorporate these new pathways and whether the associated

effluents were reported in accordance with Regulatory Guide 1.21.

d. No findings were identified.

Findings e. Groundwater Protection Initiative Program

The inspectors reviewed reported groundwater monitoring results and changes to the licensee's written program for identifying and controlling contaminated spills/leaks to groundwater.

Inspection Scope

f. No findings were identified.

Findings g. Procedures, Special Reports, and Other Documents

The inspectors reviewed Licensee Event Reports, event reports and/or special reports related to the effluent program issued since the previous inspection to identify any additional focus areas for the inspection based on the scope/breadth of problems described in these

reports.

Inspection Scope

The inspectors reviewed effluent program implementing procedures, particularly those associated with effluent sampling, effluent

monitor setpoint determinations, and dose calculations.

28 Enclosure The inspectors reviewed copies of licensee and third party (independent) evaluation reports of the effluent monitoring program since the last inspection to gather insights into the licensee's program and aid in selecting areas for inspection review (smart sampling).

h. No findings were identified.

Findings .2 Walkdowns and Observations

a. (02.02) The inspectors walked down selected components of the gaseous and liquid discharge systems to evaluate whether equipment configuration and flow paths align

ed with the documents reviewed in 02.01 above and to assess equipment material condition.

Special attention was made to identify potential unmonitored release points (such as open roof vents in boiling water reactor turbine decks, temporary structures butted against turbine, auxiliary or containment buildings), building alterations which could impact airborne or liquid effluent controls, and ventilation system leakage that

communicated

directly with the environment.

Inspection Scope

For equipment or areas associated with the systems selected for review that were not readily accessible due to radiological conditions, the inspectors reviewed the licensee's material condition surveillance records, as applicable.

The inspectors walked down filtered

-ventilation systems to assess for conditions such as degraded high-efficiency particulate air/charcoal banks, improper alignment, or system installation issues that would impact the performance or the effluent monitoring capability of the effluent system.

As available, the inspectors observed selected portions of the routine processing and discharge of radioactive gaseous effluent (including sample collection and analysis) to evaluate whether appropriate treatment equipment was used and the processing activities align

ed with discharge permits.

The inspectors determined if the licensee had

made significant changes to their effluent release points (e.g., changes subject to a 10 CFR 50.59 review or requiring

NRC approval of alternate discharge points

). As available, the inspectors observed selected portions of the routine processing and

discharge of liquid waste (including sample collection and analysis) to determine if appropriate effluent treatment equipment was being used and whether

radioactive liquid waste was being processed and discharged in accordance with procedure requirements

and aligned with discharge permits.

b. No findings were identified.

Findings

29 Enclosure .3 Sampling and Analyses

a. (02.03) The inspectors selected effluent sampling activities, consistent with smart sampling, and assessed whether adequate controls had

been implemented to ensure representative samples were obtained (e.g.

, provisions for sample line flushing, vessel recirculation, composite samplers, etc.)

Inspection Scope

The inspectors selected effluent discharges made with inoperable (declared out

-of-service) effluent radiation monitors to assess whether controls were in place to ensure compensatory sampling was performed consistent with the radiological effluent TSs/ODCM and that those controls were adequate to prevent the release of unmonitored liquid and gaseous effluents.

The inspectors determined whether the facility was routinely relying on the use of compensatory sampling in lieu of adequate system maintenance, based on the

frequency of compensatory sampling since the last inspection.

The inspectors reviewed the results of the inter-laboratory comparison program to evaluate the quality of the radioactive effluent sample analyses and assessed whether the inter-laboratory comparison program included

ha r d-to-detect isotopes as appropriate.

b. No findings were identified.

Findings .4 Instrumentation and Equipment

(02.04) a. Effluent Flow Measuring Instruments

The inspectors reviewed the methodology the licensee used

to determine the effluent stack and vent flow rates to determine if the flow rates were consistent with radiological effluent TSs/ODCM or Final Safety Analysis Report values, and that differences between assumed and actual stack and vent flow rates did not affect the results of the projected public doses.

Inspection Scope

b. No findings were identified.

Findings c. Air Cleaning Syste

ms The inspectors assessed whether surveillance test results since the previous inspection

for TS required ventilation effluent discharge systems (high

-efficiency particulate air and charcoal filtration), such as the Standby Gas Treatment System

and the Containment/Auxiliary Building Ventilation System, met TS acceptance criteria.

Inspection Scope

30 Enclosure d. No findings were identified.

Findings .5 Dose Calculations

a. (02.05) The inspectors reviewed all significant changes in reported dose values compared to the previous radiological effluent release report (e.g., a factor of 5, or increases that approach Appendix I criteria) to evaluate the factors which may have resulted in the change. Inspection Scope

The inspectors reviewed radioactive liquid and gaseous waste discharge permits to assess whether the projected doses to members of the public were accurate and based on representative samples of the discharge path.

The inspectors evaluated the methods used to determine the isotopes that were included in the source term to ensure all applicable radionuclides were included within

detectability standards. The review included the current Part 61 analyses to ensur

e hard-to-detect radionuclides were included in the source term.

The inspectors reviewed changes in the licensee's offsite dose calculations since the last inspection to evaluate whether changes were consistent with the ODCM

and Regulatory Guide 1.109. The inspectors reviewed meteorological dispersion and deposition factors used in the

ODCM and effluent dose calculations to evaluate whether appropriate factors were being used for public dose calculations.

The inspectors reviewed the latest Land Use Census to assess whether changes (e.g.,

significant increases or decreases to population in the plant environs, changes in critical exposure pathways, the location of nearest member of the public or critical receptor, etc.) had been factored into the dose calculations.

For the releases reviewed above, the inspectors evaluated whether the calculated doses (monthly, quarterly, and annual dose) were within the 10 CFR Part 50, Appendix I

, and TS dose criteria.

The inspectors reviewed, as available, records of any abnormal gaseous or liquid tank discharges (e.g., discharges resulting from misaligned

valves, valve leak

-by, etc) to ensure the abnormal discharge was monitored by the discharge point effluent monitor.

Discharges made with inoperable effluent radiation monitors, or unmonitored leakages were reviewed to ensure that an evaluation was made of the discharge to satisfy

10 CFR 20.1501 so as to account for the source term and projected doses to the public.

b. No findings were identified.

Findings

31 Enclosure .6 Groundwater Protection Initiative Implementation

a. (02.06) The inspectors reviewed monitoring results of the Groundwater Protection Initiative to determine if the licensee had implemented its program as intended and to identify any anomalous results. For anomalous results or missed samples, the inspectors assesse

d whether the licensee had identified and addressed deficiencies through its CAP. Inspection Scope

The inspectors reviewed identified leakage or spill events and entries made into

10 CFR 50.75 (g) records. The inspectors reviewed evaluations of leaks or spills

and reviewed any remediation actions taken for effectiveness. The inspectors reviewed onsite contamination events involving contamination of ground water and assessed whether the source of the leak or spill was identified and mitigated.

For unmonitored spills, leaks, or unexpected liquid or gaseous discharges, the inspectors assessed whether an evaluation was performed to determine the type and amount of radioactive material that was discharged by:

Assessing whether sufficient radiological surveys were performed to evaluate the

extent of the contamination and the radiological source term and assessing whether a survey/evaluation had been performed to include consideration of hard

-to-detect radionuclides.

Determining whether the licensee completed offsite notifications, as provided in its Groundwater Protection Initiative implementing procedures.

The inspectors reviewed the evaluation of discharges from onsite surface water bodies that contain

ed or potentially contain

ed radioactivity, and the potential for ground water leakage from these onsite surface water bodies. The inspectors assessed whether the licensee was properly accounting for discharges from these surface water bodies as part of their effluent release reports.

The inspectors assessed whether on

-site ground water sample results and a description of any significant on

-site leaks/spills into ground water for each calendar year were documented in the Annual Radiological Environmental Operating Report for the radiological environmental monitoring program or the Annual Radiological Effluent Release Report for the Radiological Effluent TSs.

For significant, new effluent discharge points (such as significant or continuing leakag

e to ground water that continued

to impact the environment if not remediated), the inspectors evaluated whether the ODCM was updated to include the new release point.

b. No findings were identified.

Findings

32 Enclosure .7 Problem Identification and Resolution

a. (02.07) Inspectors assessed whether problems associated with the effluent monitoring an

d control program were being identified by the licensee at an appropriate threshold and were properly addressed for resolution in the licensee CAP. In addition, the inspectors

evaluated the appropriateness of the corrective actions for a selected sample of problems documented by the licensee involving radiation monitoring and exposure controls. Inspection Scope

b. No findings were identified.

Findings 2RS7 Radiological Environmental Monitoring ProgramThis inspection constituted one complete sample as defined in IP

71124.07-05. (71124.07)

.1 Inspection Planning

a. (02.01) The inspectors reviewed the annual radiological environmental operating reports and the results of any licensee assessments since the last inspection to assess whether the radiological environmental monitoring program was implemented in accordance with the TSs and ODCM. This review included reported changes to the OD

CM with respect to environmental monitoring, commitments in terms of sampling locations, monitoring and measurement frequencies, land use census, inter

-laboratory comparison program, and analysis of data.

Inspection Scope

The inspectors reviewed the ODCM to identify locations of environmental monitoring stations. The inspectors reviewed the Final Safety Analysis Report for information regarding the environmental monitoring program and meteorological monitoring instrumentation.

The inspectors reviewed quality assurance audit results of the program to assist in

choosing inspection "smart samples" and audits and technical evaluations performed on the vendor laboratory program.

The inspectors reviewed the annual effluent release report and the 10 CFR Part 61, "Licensing Requirements for Land Disposal of Radioactive Waste," report, to determine

if the licensee was sampling, as appropriate, for the predominant and dose

-causing radionuclides likely to be released in effluents.

b. No findings were identified.

Findings

33 Enclosure .2 Site Inspection

a. (02.02) The inspectors walked down select air sampling stations and thermoluminescent dosimeter monitoring stations to determine whether they were located as described in the ODCM and to determine the equipment material condition.

Consistent with smart sampling, the air sampling stations were selected based on the locations with the highest X/Q, D/Q wind sectors, and

thermoluminescent dosimeters were selected based on the most risk

-significant locations (e.g., those that have the highest potential for public dose impact).

Inspection Scope

For the air samplers and thermoluminescent dosimeters selected, the inspectors

reviewed the calibration and maintenance records to evaluate whether they demonstrated adequate operability of these components. Additionally, the review included the calibration and maintenance records of select composite water samplers.

The inspectors assessed whether the licensee had initiated sampling of other appropriate media upon loss of a required sampling station.

The inspectors observed the collection and preparation of environmental samples from different environmental media (e.g., ground and surface water, milk, vegetation, sediment, and soil) as available to determine if environmental sampling was representative of the release pathways as specified in the ODCM and if sampling techniques were in accordance with procedures.

Based on direct observation and review

of records, the inspectors assessed whether the meteorological instruments were operable, calibrated, and maintained in accordance

with guidance contained in the Final Safety Analysis Report;

NRC Regulatory Guide 1.23, "Meteorological Monitoring Programs for Nuclear Power Plants;

" and licensee procedures. The inspectors assessed whether the meteorological data readout and recording instruments in the control room and, if applicable, at the tower were operable.

The inspectors evaluated whether missed and/or anomalous environmental samples were identified and reported in the annual environmental monitoring report. The inspectors selected events that involved a missed sample, inoperable sampler, lost

thermoluminescent dosimeter, or anomalous measurement to determine if the licensee had identified the cause and had implemented corrective actions. The inspectors reviewed the licensee's assessment of any positive sample results (i.e., licensed radioactive material detected above the lower limits of detection) and reviewed the associated radioactive effluent release data that was the source of the released material.

The inspectors selected structures, systems, or components that involve

d or could reasonably involve licensed material for which there was a credible

mechanism for licensed material to reach ground water, and assessed whether the licensee had implemented a sampling and monitoring program sufficient to detect leakage of these structures, systems, or components to ground water.

34 Enclosure The inspectors evaluated whether records, as required by 10 CFR 50.75(g), of leaks, spills, and remediation since the previous inspection were retained in a retrievable manner. The inspectors reviewed any significant changes made by the licensee to the ODCM as the result of changes to the land census, long

-term meteorological conditions (3

-year average), or modifications to the sampler stations since the last inspection. The inspectors

reviewed technical justifications for any changed sampling locations to evaluate whether the licensee performed the reviews required to ensure that the changes did not affect the ability to monitor the impact

of radioactive effluent releases on the environment.

The inspectors assessed whether the appropriate detection sensitivities with respect to

TSs/ODCM were used for counting samples (i.e., the samples met the TSs/ODCM required lower limits of detection). The inspectors reviewed quality control charts for

maintaining radiation measurement instrument status and actions taken for degrading detector performance. The licensee used

a vendor laboratory to analyze the radiological environmental monitoring program samples so the inspectors reviewed the results of the

vendor's quality control program, including the interlaboratory comparison, to assess th

e adequacy of the vendor's program.

The inspectors reviewed the results of the licensee's interlaboratory comparison program to evaluate the adequacy of environmental sample analyses performed by the licensee. The inspectors assessed whether the interlaboratory comparison test included the media/nuclide mix appropriate for the facility. If applicable, the inspectors reviewed the licensee's determination of any bias to the data and the overall effect on the

radiological environmental monitoring program.

b. No findings were identified.

Findings .3 Identification and Resolution of Problems

a. (02.03) The inspectors assessed whether problems associated with the radiological environmental monitoring program were being identified by the licensee at an

appropriate threshold and were properly addressed for resolution in the licensee's CAP. Additionally, the inspectors

assessed the appropriateness of the corrective actions for a selected sample of problems documented by the licensee that involved the radiological environmental monitoring program.

Inspection Scope

b. No findings were identified.

Findings 2RS8 Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and TransportationThis inspection constituted one complete sample as defined in IP 71124.08

-05. (71124.08)

35 Enclosure .1 Inspection Planning

a. (02.01) The inspectors reviewed the solid radioactive waste system description in the Final Safety Analysis Report, the process control program, and the recent radiological effluent release report for information on the types, amounts, and processing of radioactive waste disposed.

Inspection Scope

The inspectors reviewed the scope of any quality assurance audits in this area since the last inspection to gain insights into the licensee's performance and inform the "smart sampling" inspection planning.

b. No findings were identified.

Findings .2 Radioactive Material Storage

a. (02.02) The inspectors selected areas where containers of radioactive waste were stored, and evaluated whether the containers were labeled in accordance with 10 CFR 20.1904, "Labeling Containers," or controlled in accordance with 10 CFR 20.1905, "Exemptions to Labeling Requirements," as appropriate.

Inspection Scope

The inspectors assessed whether the radioactive material storage areas were controlled

and posted in accordance with the requirements of 10 CFR Part 20, "Standards for Protection against Radiation." For

materials stored or used in controlled or unrestricted areas, the inspectors evaluated whether they were secured against unauthorized

removal and controlled in accordance with 10 CFR 20.1801, "Security of Stored Material," and 10 CFR 20.1802, "Control of Material Not in Storage," as appropriate.

The inspectors evaluated whether the licensee established a process for monitoring the impact of long term storage (e.g., buildup of any gases produced by waste decomposition, chemical reactions, container deformation, loss of container integrity, or

re-release of free

-flowing water) that was sufficient to identify potential unmonitored, unplanned releases or nonconformance with waste disposal requirements.

The inspectors selected containers of stored radioactive material, and inspected the containers

for signs of swelling, leakage, and deformation.

b. No findings were identified.

Findings .3 Radioactive Waste System Walkdown

a. (02.03) The inspectors walked down accessible portions of select radioactive waste processing systems to assess whether the current system configuration and operation agreed with Inspection Scope

36 Enclosure the descriptions in the Final Safety Analysis Report, ODCM, and process control program. The inspectors reviewed administrative and/or physical controls (i.e., drainage and isolation of the system from other systems) to assess whether the equipment which wa

s not in service or abandoned in place would contribute to an unmonitored release path and/or affect operating systems or be a source of unnecessary personnel exposure. The inspectors assessed whether the licensee reviewed the safety significance of systems and equipment abandoned in place in accordance with 10 CFR 50.59, "Changes, Tests, and Experiments

." The inspectors reviewed the adequacy of changes made to

the radioactive waste processing systems since the last inspection. The inspectors evaluated whether

changes from what was described in the Final Safety Analysis Report were reviewed and documented in accordance with 10 CFR 50.59, as appropriate and to assess the impact on radiation doses to members of the public.

The inspectors selected processes for transferring radioactive waste resin and/or sludge discharges into shipping/disposal containers and assessed whether the waste stream mixing, sampling procedures, and methodology for waste concentration averaging were consistent with the process control program, and provided representative samples of the waste product for the purposes of waste classification as described in 10 CFR 61.55, "Waste Classification

." For those systems that provide

d tank recirculation, the inspectors evaluated whether the tank recirculation procedures provided sufficient mixing.

The inspectors assessed whether the licensee's process control program correctly described the current methods and procedures for dewatering and waste stabilization (e.g., removal of freestanding liquid).

b. No findings were identified.

Findings .4 Waste Characterization and Classification

a. (02.04) The inspectors selected the following radioactive waste streams for review:

Inspection Scope

Primary Resin;

Secondary Resin;

Secondary Radwaste Filter; and

Dry Active Waste (DAW).

For the waste streams listed above, the inspectors assessed whether the licensee's radiochemical sample analysis results (i.e., "10 CFR Part 61" analysis) were sufficient to support radioactive waste characterization as required by 10 CFR Part 61, "Licensing Requirements for Land Disposal of Radioactive Waste." The inspectors evaluated whether the licensee's use of scaling factors and calculations to account for difficult

-to-

37 Enclosure measure radionuclides was technically sound and based on current 10 CFR Part 61 analyses for the selected radioactive waste streams.

The inspectors evaluated whether changes to plant operational parameters were taken into account to: (1) maintain the validity of the waste stream composition data between the annual or biennial sample analysis update; and (2) assure that waste shipments

continued to meet the requirements of 10 CFR Part 61 for the waste streams selected above. The inspectors evaluated whether the licensee had established and maintained an adequate quality assurance program to ensure compliance with the waste classification and characterization requirements of 10 CFR 61.55 and 10 CFR 61.56, "Waste Characteristics." b. No findings were identified.

Findings .5 Shipment Preparation

a. (02.05) The inspectors observed shipment packaging, surveying, labeling, marking, placarding, vehicle checks, emergency instructions, disposal manifest, shipping papers provided to the driver, and licensee verification of shipment readiness. The inspectors assessed

whether the requirements of applicable transport cask certificate

s of compliance had been met. The inspectors evaluated whether the receiving licensee was authorized to

receive the shipment packages. The inspectors evaluated whether the licensee's procedures for cask

loading and closure were consistent with the vendor's current approved procedures.

Inspection Scope

The inspectors observed radiation workers during the conduct of radioactive waste processing and radioactive material shipment preparation and receipt activities. The inspectors assessed whether the shippers were knowledgeable of the shipping regulations and whether shipping personnel demonstrated adequate skills to accomplish the package preparation requirements for public transport with respect to

the licensee's response to NRC Bulletin 79

-19, "Packaging of Low

-Level Radioactive Waste for Transport and Burial," dated August 10, 1979; and Title 49 CFR Part 172, "Hazardous Materials Table, Special Provisions, Hazardous Materials Communication, Emergency Response Information, Training Requirements, and Security Plans," Subpart H, "Training."

Due to limited opportunities for direct observation, the inspectors reviewed the technical instructions presented to workers during routine training. The inspectors assessed

whether the licensee's training program provided training to personnel responsible for the conduct of radioactive waste processing

and radioactive material shipment preparation activities.

b. No findings were identified.

Findings

38 Enclosure .6 Shipping Records

a. (02.06) The inspectors evaluated whether the shipping documents indicated the proper shipper name; emergency response information and a 24

-hour contact telephone number; accurate curie content and volume of material; and appropriate waste classification,

transport index, and UN number for the following radioactive shipments:

Inspection Scope

Shipment RWS10

-011; Dewatered Bead Resin; low specific

activity (LSA

-II); Shipment RWS10

-013; DAW Trash and TR Pond Sludge; low specific activity (LSA-II); Shipment RWS10

-012; DAW Trash; low specific activity (LSA

-II); Shipment RMS09

-094; Rx Vessel Dosimetry; Type A Package; and

Shipment RMS11

-078; Dirty Laundry; low specific activity (LSA

-II). Additionally, the inspectors assessed whether the shipment placarding was consistent with the information in the shipping documentation.

b. Findings Introduction

A self-revealed finding of very

low safety significance (Green) and an associated NCV of 10 CFR 71.5, "Transportation of Licensed Material,"

was identified

when licensee personnel failed to comply with 49 CFR 172.203(c) and shipped packages of radioactive material with transport manifests that did not document all applicable hazardous substances. Description IR 1221229; RWS 11

-006 Contained Un

-Manifested Asbestos;

On multiple dates, the licensee shipped containers of radioactive material to a waste processor with incomplete information on the transport manifest. Specifically, the transport manifest that accompanied the shipments failed to identify hazardous materials, including asbestos, lead, and other chemicals that were contained in the packages. Upon arrival at the waste processor's facility, the waste processor identified the non-conformances in the shipping

containers and notified the licensee. Follow-up actions by the licensee included performing a revised characterization of the shipped packages. The revised radiological characterization identified negligible impact relative to the initial radiological assessment and package characterization. This event was documented in the licensee's CAP as: IR 1173307; RWS 10

-013 Contained Unapproved Mixed Waste;

IR 928393; Non

-Conforming Metal Shipped to Bear

Creek Processing;

IR 1015646; Non

-Conforming Waste Found in Radwaste Shipment; and

IR 1067394; Non

-Conforming Radioactive Waste in Shipment.

39 Enclosure Immediate corrective actions included providing a corrected copy of the transport manifest to the waste processor. Additionally, the licensee initiated IR 1285148

to evaluate the human performance issues associated with th

e shipping non-conformance

s. Further, the licensee placed locks on the shipping containers

to control items placed in the packages

and t o ensure that the manifest accurately represented

the hazards contained in the shipping package.

AnalysisThis finding has a cross

-cutting aspect in the Work Control component of the Human

Performance cros

s-cutting area H.3(b) since the waster shipper

failed to coordinate work activities by incorporating actions to address the impact of the work on different job

activities, and the need for work groups to maintain interfaces with offsite organizations, and communicate, coordinate, and cooperate with each other during activities in which interdepartmental coordination is necessary to assure adequate human performance

. Specifically, these events occurred because the radioactive material

shipper did not control the items

placed in the waste packages and was not present when the boxes were loaded.

The failure to completely identify all required package contents on a transport manifest was a performance deficiency. The finding wa

s determined to be more than minor because it was associated with the Program and Process attribute of the Public Radiation Safety

Cornerstone and adversely affected the cornerstone objective

of ensuring the adequate protection of public health and safety from exposure to radioactive materials released into the public domain as a result of routine civilian nuclear reactor operation, in that, providing incorrect information, as part of hazard communication, could impact the actions of response personnel. The finding involved an occurrence of the licensee's radioactive material transportation program that wa

s contrary to NRC regulatory requirements. The inspectors determined that the finding could be evaluated using the SDP in accordance with IMC 0609, "Significance Determination Process," Appendix D, "Public Radiation Safety Significance Determination Process." Using the Public Radiation Safety SDP, the inspector

s determined

(1) radiation limits were not exceeded; (2) there was no breach of a package during transit; (3) it did not involve a certificate of compliance issue; (4) it was not a low level burial ground nonconformance; and (5) it did not involve a failure to make notifications or provide emergency information.

As a result, the finding screened as having very low safety significance (Green).

EnforcementContrary to the above, between May 10, 2010 and May 26, 2011, the licensee failed to list relevant hazardous materials on the transport manifest for a shipment also containing DAW. This violation was entered into the licensee's CAP as IR 1285148. Because this violation was of very low

safety significance and it was entered into the licensee's CAP , this violation

is being treated as an NCV, consistent with Section 2.3.2

of the NRC Enforcement Policy

. (NCV 05000454/2011005

-04 , Failure to Identify Hazardous Materials on Transportation Manifest) : Title 10 CFR 71.5, "Transportation of Licensed Material," requires licensees to comply with the Department of Transportation (DOT) regulations in

49 CFR Parts 170 through 189 relative to the transportation of licensed material. Title 49 CFR 172.203

, "Additional Description Requirements," required, in part, that hazardous materials be listed on the transport manifest.

40 Enclosure .7 Identification and Resolution of Problems

a. (02.07) The inspectors assessed whether problems associated with radioactive waste processing, handling, storage, and transportation, were being identified by the licensee at an appropriate

threshold, were properly characterized, and were properly addressed for resolution in the licensee CAP. Additionally, the inspectors evaluated whether the corrective actions were appropriate for a selected sample of problems documented by the licensee that involve radioactive waste processing, handling, storage, and transportation.

Inspection Scope

The inspectors reviewed results of selected audits performed since the last inspection of

this program and evaluated the adequacy of the licensee's corrective actions for issue

s identified during those audits.

b. No findings were identified.

Findings 4. OTHER ACTIVITIES

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and Emergency Preparedness

4OA1 Performance Indicator Verification

.1 (71151) a. Reactor Coolant

System Leakage

The inspectors sampled licensee submittals for the Unit 1 and Unit 2 RCS Leakage Performance Indicator (PI) for the period from the third quarter 2010 through the second quarter 2011.

To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in Nuclear Energy Institute (NEI) 99

-02, "Regulatory Assessment Performance Indicator Guideline," Revision 6, dated October 2009 , was used. The inspectors reviewed the licensee's operator logs, RCS leakage tracking data, issue reports, event reports and

NRC Integrated Inspection Reports for the period of June 2010 through June 2011

to validate the accuracy of the submittals. The inspectors also reviewed the licensee's issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator. Documents reviewed are listed in the Attachment.

Inspection Scope

This inspection constituted two RCS leakage samples as defined in IP

71151-05. b. No findings were identified.

Findings

41 Enclosure .2 a. Unplanned Transients Per 7000 Critical Hours

The inspectors sampled licensee submittals for the Unplanned Transients per 7000 Critical Hours performance indicator for Unit 1 and Unit 2

for the period from the

second quarter of 2010 through the 3

rd quarter of 2011. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in NEI 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 6, dated

October 2009 , was used. The inspectors reviewed the licensee's operator narrative logs, issue reports, maintenance rule records, event reports and NRC Integrated

Inspection

Reports for the period of

April 2010 through September 2011 to validate the accuracy of the submittals. The inspectors also reviewed the licensee's issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator

. Documents reviewed are listed in the Attachment.

Inspection Scope

This inspection constituted two unplanned transients per 7000 critical hours samples as defined in IP

71151-05. b. No findings were identified.

Findings .3 a. Safety System Functional Failures

The inspectors sampled licensee submittals for the Safety System Functional Failures performance indicator

for Unit 1 and Unit 2

for the period from the second quarter of 2010 through the third quarter of 2011.

To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in NEI 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 6, dated October 2009, and NUREG

-1022, "Event Reporting Guidelines

10 CFR 50.72 and 50.73" definitions and guidance

, were used. The inspectors reviewed the licensee's operator narrative logs, operability assessments, maintenance rule records, maintenance work orders, issue reports, event reports and NRC Integrated Inspection

Reports for the period of June 2010 through September 2011

to validate the accuracy of the submittals. The inspectors also reviewed the licensee's issue report database to

determine if any problems had been identified with the PI data collected or transmitted for this indicator. Documents reviewed

are listed in the Attachment

. Inspection Scope

This inspection constituted two safety system functional failures samples as defined in

IP 71151-05. b. No findings were identified.

Findings

42 Enclosure .4 a. Reactor Coolant System Specific Activity

The inspectors sampled licensee submittals for the

RCS specific activity PI for Unit

1 and Unit 2 for the period from the 4th quarter of 2010 through the 3rd

quarter of 2011. The inspectors used PI definitions and guidance contained in NEI 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 6, dated October 2009 to determine the accuracy of the PI data reported during those periods. The inspectors reviewed the licensee's reactor coolant system

chemistry samples, TS requirements, issue reports, event reports

, and NRC Integrated Inspection Reports for the period of the 4th quarter 2010 through the 3rd quarter of 2011 to validate the accuracy of the submittals. The inspectors also reviewed the licensee's issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator. In addition to record reviews, the inspectors observed a chemistry technician obtain and analyze a reactor coolant system sample. Documents reviewed are listed in the Attachment.

Inspection Scope

This inspection constituted two

RCS specific activity samples as defined in IP

71151-05. b. No findings were identified.

Findings .5 a. Mitigating Systems Performance Index

- Heat Removal System

The inspectors sampled licensee submittals for the Mitigating Systems Performance

Index (MSPI) - Heat Removal System performance indicator

for Unit 1 and Unit 2 for the period from the

fourth quarter of 2010 through the third quarter of 2011. To determine the accuracy of the PI data

reported during those periods, PI definitions and guidance contained in NEI 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 6, dated October 2009 , was used. The inspectors reviewed the licensee's operator narrative logs, issue reports, event reports, MSPI derivation reports, and NRC Integrated I

Rs for the period of

October 2010 through September 2011

to validate the accuracy of the submittals. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, that the change was in accordance with applicable NEI

guidance. The inspectors also reviewed the licensee's issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator. Documents reviewed are listed in the Attachment

. Inspection Scope

This inspection constituted two MSPI heat removal system samples as defined in

IP 71151-05. b. No findings were identified.

Findings

43 Enclosure .6 a. Mitigating Systems Performance Index

- Cooling Water Systems

The inspectors sampled licensee submittals for the MSPI - Cooling Water Systems performance indicator for Unit 1 and Unit 2

for the period from the fourth quarter of 2010 through the third quarter of 2011. To determine the accuracy of the PI data reported during those periods, PI definitions

and guidance contained in NEI 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 6, dated October 2009 , was used. The inspectors

reviewed the licensee's operator narrative logs, issue reports, MSPI derivation reports, event reports and NRC Integrated Inspection

Reports for the period of October 2010 through September 2011

to validate the accuracy of the submittals. The inspectors reviewed the MSPI component risk coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, whether the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensee's issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator. Documents reviewed are listed in the Attachment.

Inspection Scope

This inspection constituted two MSPI cooling water system samples as defined in

IP 71151-05. b. No findings were identified.

Findings .7 a. Mitigating Systems Performance Index

- High Pressure Injection Systems

The inspectors sampled licensee submittals for the MSPI - High Pressure Injection Systems performance indicator for Unit 1 and Unit 2 for the period from the fourth quarter of 2010 through the third quarter of 2011. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in NEI 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 6, dated October 2009 , were used. The inspectors reviewed the licensee's operator narrative logs, issue reports, MSPI derivation reports, event reports and NRC Integrated Inspection

Reports for the period of

October 2010 through September of 2011

to validate the accuracy of the submittals. The inspectors reviewed the MSPI component risk

coefficient to determine if it had changed by more than 25 percent in value since the previous inspection, and if so, that the change was in accordance with applicable NEI guidance. The inspectors also reviewed the licensee's issue report database to determine if any problems had been identified with the PI data collected or transmitted

for this indicator. Documents reviewed

are listed in the Attachment.

Inspection Scope

This inspection constituted two MSPI high pressure injection system samples as defined in IP 71151-05. b. No findings were identified.

Findings

44 Enclosure .8 a. Occupational Exposure Control Effectiveness

The inspectors sampled licensee submittals for the occupational radiological occurrences PI for the period from the fourth quarter of 2010 through the 3rd

quarter of 2011. To determine the accuracy of the PI data reported during these periods, t

he inspectors used PI definitions and guidance contained in NEI 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 6, dated October 2009. The inspectors reviewed the licensee's assessment of the PI for occupational radiation safety to determine if indicator

-related data was adequately assessed and reported. To assess the adequacy of the licensee's PI data collection and analyses, the inspectors discussed with radiation protection staff, the scope

, and breadth of its data review and the results

of those reviews. The inspectors independently reviewed electronic personal dosimetry dose rate and accumulated dose alarms and dose reports and the dose assignments for any intakes that occurred during the time period reviewed to determine if there were

potentially unrecognized occurrences. The inspectors also conducted walkdowns of numerous locked high and very high radiation area entrances to determine the adequacy of the controls in place for these areas. Documents reviewed are listed in the Attachment. Inspection Scope

This inspection constituted one occupational exposure control effectiveness sample as defined in IP

71151-05. b. No findings were identified.

Findings .9 a. Radiological Effluent Technical Specification/Offsite Dose Calculation Manual Radiological Effluent Occurrences The inspectors sampled licensee submittals for the radiological effluent TS/ODCM

radiological effluent occurrences PI for the period from the fourth quarter of 2010 through the third quarter of 2011. To determine the accuracy of the PI data reported during these periods, the inspectors used PI definitions and guidance contained in NEI 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 6, dated October 2009. The inspectors reviewed the licensee's issue report

database and selected individual reports generated since this indicator was last reviewed to identify any potential occurrences such as unmonitored, uncontrolled, or improperly calculated effluent releases that may have impacted offsite dose. The inspectors reviewed gaseous effluent summary data and the results of associated offsite dose calculations for selected dates between the fourth quarter of 2010 through the third quarter of 2011 to determine if indicator results were accurately reported. The inspectors also reviewed the

licensee's methods for quantifying gaseous and liquid effluents and determining effluent dose. Documents reviewed are listed in the Attachment

. Inspection Scope

45 Enclosure This inspection constituted one Radiological Effluent TS/ODCM radiological effluent

occurrences sample as defined in IP 71151 05.

b. No findings were identified.

Findings 4OA2 Identification and Resolution of ProblemsCornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical Protection

(71152) .1 a. Routine Review of Items Entered into the Corrective Action Program

As part of the various baseline inspection procedures discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that they were being entered into the licensee's CAP at an appropriate threshold, that adequate attention was being given to timely corrective actions, and that adverse trends were identified and addressed. Attributes reviewed included: the complete and accurate identification of the problem; that timeliness was commensurate with the safety significance; that evaluation and disposition of performance issues, generic implications, common causes, contributing factors, root causes, extent

-of-condition reviews, and previous occurrence reviews were proper and adequate; and that the classification, prioritization, focus, and timeliness of corrective actions were commensurate with safety and sufficient to prevent recurrence of the issue. Minor issues entered into the licensee's CAP as a result of the inspectors' observations

are included in the attached

List of Documents Reviewed. Inspection Scope These routine reviews for the identification and resolution of problems did not constitute any additional inspection samples. Instead, by procedure they were considered an integral part of the inspections performed during the quarter and documented in Section 1 of this report.

b. No findings were identified.

Findings .2 a. Daily Corrective Action Program Reviews

In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow

-up, the inspectors

performed a daily screening

of items entered into the licensee's CAP. This review was accomplished through inspection of the station's daily condition report packages.

Inspection Scope

46 Enclosure These daily reviews were performed by procedure as part of the inspectors' daily plan

t status monitoring activities and, as such, did not constitute any separate inspection samples. b. No findings were identified.

Findings .3 a. Selected Issue Follow

-Up Inspection: Licensee Issue Report on Auxiliary Feedwater System Crosstie Modification

The inspectors performed a review of the item below that was identified by an NRC inspector at a different but similar facility

Inspection Scope Auxiliary Feedwater System Modification.

This review constituted one in

-depth problem identification and resolution sample as defined in IP

71152-05. b. No findings were identified.

Findings .4 a. Annual Sample: Review of Operator Workarounds

The inspectors evaluated the licensee's implementation of their process used to identify, document, track, and resolve operational challenges. Inspection activities included, but were not limited to, a review of the cumulative effects of the operator workarounds

(OWAs) on system availability and the potential for improper operation of the system, for potential impacts on multiple systems, and on the ability of operators to respond to plant transients or accidents.

Inspection Scope The inspectors performed a review of the cumulative effects of OWAs. The documents listed in the

Attachment were reviewed to accomplish the objectives of the inspection procedure. The inspectors reviewed both current and historical operational challenge records to determine whether the licensee was identifying operator challenges at an appropriate threshold, had entered them into their CAP , and proposed or implement

ed appropriate and timely corrective actions which addressed each issue. Reviews were

conducted to determine if any operator challenge could increase the possibility of an Initiating Event, if the challenge was contrary to training, required a change from

long-standing operational practices, or created the potential for inappropriate compensatory actions. Additionally, all temporary modifications were reviewed to identify any potential effect on the functionality of Mitigating Systems, impaired access to equipment, or required equipment uses for which the equipment was not designed. Daily plant and equipment status logs, degraded instrument logs, and operator aids or tools being used to compensate for material deficiencies were also assessed to identify

any potential sources of unidentified operator workarounds.

47 Enclosure This review constituted one operator workaround

annual inspection sample

as defined in

IP 71152-05. b. No findings were identified.

Findings 4OA3 Follow-Up of Events and Notices of Enforcement Discretion

.1 (71153) The Licensee Event Report

(LER) involved a Unit 2 DG that was unknowingly inoperable for approximately

6 months due to lo

ose bolting on the upper lubricating oil cooler. During a routine surveillance on November 17, 2010, a significant oil leak was identified by the equipment o

perator. The DG was shut

down before damage could occur. The licensee determined that a bolted flanged connection was misaligned during

reinstallation following maintenance in January of 2010.

(Closed) Licensee Event Report 05000455/2011

-001, Revision 0 and Revision 1, "Unit 2 Emergency Diesel Generator Inoperable for Longer Than Allowed by Technical Specifications Due to Inadequate Work Instructions"

NRC Follow

-Up inspection 05000455/2011011 determined that the issue was an apparent violation and a White Finding (EA

-11-014). The

IR was issued February 11, 2011. On October 4, 2011, an

NRC IP 95001 Supplemental I

R was issued documenting the closure of finding 05000455/2011011

-01. As the enforcement actions have b

een issued, and the Supplemental Inspection has been completed with no significant issues identified, these LERs are closed.

.2 The LER involved a licensee

-identified mistaken plugging of a pressure sensor inside of containment during the previous refueling outage. The plugged was placed during a routine surveillance on September 28, 2011

and on October 13, 2011, licensee personnel determined that while the instrument indicated that Unit 2 containment

pressure was within limits, that, in fact containment pressure was above the TS limit. A containment entry was made, the plug was removed, containment pressure was reduced and the peak pressure was determined to be approximately 1.91 pounds per square inch gauge (psig). The TS allowed value was 1.0 psig and the amount of time that the pressure could be above the limit was 1

hour with the plant required to be shut

down within the following 42 hours4.861111e-4 days <br />0.0117 hours <br />6.944444e-5 weeks <br />1.5981e-5 months <br />. By the time the situation was identified, understood

, and corrected a total time of 95 hours0.0011 days <br />0.0264 hours <br />1.570767e-4 weeks <br />3.61475e-5 months <br /> and 48 minutes had elapsed.

(Closed) Licensee Event Report 05000455/2011

-002, Revision 0, "Containment Pressure Not Within Limits Longer than Allowed By Technical Specifications Due to Personnel Error"

The licensee determined and the inspectors verified that the licensee's safety margin between peak containment pressure and the initial maximum allowed pressure was

10 psig. The technicians' error and the delay in correcting the error resulted in 0.91 psig of the 10 psig margin being used. There was a minor adverse safety consequence due to the licensee personnel's error.

The technicians' error identified by the licensee resulted in a minor failure to comply with

TS 3.6.4, "Containment Pressure". This LER is closed.

48 Enclosure 4OA6 .1 Management Meetings

O n January 12, 2012, the inspector

s presented the inspection results to

Mr. B. Youman, and other members of the licensee staff. The licensee acknowledged the issues presented. The inspectors confirmed that none of the potential report input discussed was considered proprietary.

Exit Meeting Summary .2 Interim exits were conducted for:

Interim Exit Meetings

The results of an Operator Licensing inspection with the Lead Operations Training staff instructor, Mr. M. McCue, via telephone

on December 8, 2011.

The results of an annual review of Emergency Action Level and Emergency Plan changes with the Emergency Preparedness

Coordinator, Mr.

R. Kartheiser, via telephone on December 7, 2011.

The results of Occupational and Public Radiation Safety programs inspections with the Site Vice President, Mr. T. Tulon, on November 10, 2011 and with the Acting Plant Manager, E. Hernandez, on December 28, 2011

. The licensee acknowledged the issues presented. The inspectors confirmed that none of the potential report input discussed was considered proprietary.

Proprietary material received during the inspection was returned to the licensee.

4OA7 The following violation of very low safety significance was identified by the licensee. The violation met the criteria of Section VI of the NRC Enforcement Policy

for being dispositioned

as a Non-Cited Violation

. Licensee-Identified Violations

.1 Technical Specification 5.5.1 states that the ODCM shall contain the methodology and parameters used in the calculation of offsite doses resulting from radioactive gaseous and liquid effluents, and in the calculation of gaseous and liquid monitoring alarm

and trip setpoints.

Effluent Monitors Alarms Setpoints Incorrectly Established

Contrary to the above, on August 26, 2010, the licensee identified a potential

for non-conservative alarm setpoints for effluent monitors. Subsequently, the licensee

calculated new setpoints for these monitors using the methodology prescribed in the ODCM and determined that the previous alarm setpoints were incorrectly established

and were non

-conservative (too high). The inspectors determined that this finding was of more than minor significance because it was

similar to Example 6.c in IMC 0612

, Appendix E, "Example of Minor Issues". Specifically, the effluent monitors with its alarm

set points would have failed to perform its intended function (i.e., trip or isolation function) to prevent an instantaneous effluent release in excess of the applicable

TS instantaneous dose rate limits for gases. In accordance with IMC 0609, Appendix D,

49 Enclosure "Public Radiation Safety," the inspectors determined the violation to be of very low safety significance, (Green) because

the dose impact to a member of the public from the radiological release was less than the dose values in Appendix I to 10 CFR Part 50 and

10 CFR 20.1301(e). This violation of TS 5.5.1 is being treated as a NCV consistent with Section 2.3.2 of the NRC Enforcement Policy.

The licensee entered this issue into their

CAP as IR 1106461.

ATTACHMENT: SUPPLEMENTAL INFORMATION

1 Attachment

SUPPLEMENTAL INFORMATION KEY POINTS OF CONTAC

T T. Tulon, Site Vice President

Licensee B. Youman, Plant Manager

D. Coltman, Operations Manager

J. Feimster, Design Engineering Manager

D. Damptz, Acting Maintenance Director

S. Swanson, Nuclear Oversight Manager

R. Gayheart, Training Director

B. Barton, Radiation Protection Manager

K. Anderson, Acting Radiation Protection Manager

A. Creamean, Chemistry Manager

D. Gudger, Regulatory Assurance Manager

R. Cameron, Licensed Operator Requalification Lead

E. Duncan , Chief, Branch 3, Division of Reactor Projects

Nuclear Regulatory Commission

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

05000454/2011005

-001 Opened and Closed

NCV Failure to Identify Voided Sections of AF Piping

(Section 1R15)

05000455/2011005

-001 NCV Failure to Identify Voided Sections of AF Piping

(Section 1R15)

05000454/2011005

-002 NCV High Energy Line Break Operability Evaluation

(Section 1R15)

05000455/2011005

-002 NCV High Energy Line Break Operability Evaluation

(Section 1R15)

05000454/2011005

-003 URI Use of TLDs May Not be Consistent with the Methods

Used by the NVLAP Accreditation Process (Section 2RS4)

05000455/2011005

-003 URI Use of TLDs may not be consistent with the methods used

by the NVLAP accreditation process (Section 2RS4)

05000454/2011005

-004 NCV Failure to Identify Hazardous Materials on Transportation

Manifest (Section 3RS8)

2 Attachment

05000455/2011011

-00 Closed LER Unit 2 Emergency Diesel Generator Inoperable for Longer Than Allowed by Technical Specifications Due to Inadequate Work Instructions, Revision 0

05000455/2011011

-01 LER Unit 2 Emergency Diesel Generator Inoperable for Longer Than Allowed by Technical Specifications

Due to Inadequate Work Instructions, Revision

3 Attachment

LIST OF DOCUMENTS REVIEWED The following is a list of documents reviewed during the inspection. Inclusion

on this list does not imply that the NRC inspectors reviewed the documents in their entirety, but rather, that selected sections of portions of the documents were evaluated as part of the overall inspection effort. Inclusion of a document on this list does not imply NRC acceptance of the document or any part of it, unless this is stated in the body of the inspection report.

- IR 1067880; Byron 2010/2011 Winter Readiness Critique, March 30, 2011

Section 1R01: Adverse Weather Protection (Quarterly)

- IR 1186291; 2010/2011 Winter Readiness Critique, March 11, 2011

- IR 1193076; Action Tracking Process Versus Work Control Process, December

2, 2010 - IR 1238947; SX Chemical Feed Lines Need Insulating, July 12, 2011

- IR 1262839; Winter Readiness Work Rescheduled, September 14, 2011

- IR 1265348; Unable to Resolve Parts Required Issue, September 14, 2011

- IR 1265934; Winter Readiness Challenge

- No CST Heaters Available, September

21, 2011 - IR 1280434; Switchyard Winter Readiness PM, October 24, 2011

- IR 1280750; Freeze Protection

- CWPH Louvers LV48, 142 Stuck Open, October

24, 2011 - IR 1280755; Freeze Protection

- Electric Heater 0VV37C Fan Motor, October

24, 2011 - IR 1280755; Freeze Protection: Electric Heater 0VV37C Fan Motor, October 24, 2011

- IR 1280757; 0VH09Y

- Damper Stuck Open, October 24, 2011

- IR 1281870; Roof Access Hatch Will Not Remain Closed, October 26, 2011

- IR 1285676; Winter Readiness Walkdown, November 2, 2011 - IR 1286684; 0VT17J LV

-82 Has a Louver Broke Preventing Set From Closing, November 5, 2011 - IR 1286686; 0VT11J LV

-8 Has a Set of Louvers Not Fully closed, November

5, 2011 - IR 1286687; 0VT16J LV

-80 Has a Broken Louver Preventing Set From Closing, November 5, 2011 - IR 1286688; 0VT13J LV

-17 Has 2 Sets of Louvers Not Fully Closed, November

5, 2011 - IR 1286689;

0VT18J LV-83 Has Broken Louvers Preventing Set From Closing, November 5, 2011 - IR 1286693; 0VT20J LV

-86 Sets of Louvers Not Fully Closed, November 5, 2011

- IR 1286904; 0VT07J LV

-4 Has Broken Louvers, November 5, 2011

- IR 1286907; 0VT08J LV

-5 Has 2 Sets of Louvers Not Fully Closed, November 5, 2011

- IR 1286908; 0VT10J LV

-7 Has One Broken Louver, November 5, 2011

- IR 1286910; 0VT14J LV

-18 Has a Set of Louvers Not Fully Closed, November

5, 2011 - IR 1286912; 0VT12J LV

-9 Has Broken Louvers and Sets Not Fully Closed, November 5, 2011 - IR 1289988; Freeze Protection Concern, November 13, 2011

- IR 1293508; Winter Readiness System Review Work Removed From 2011,

November 15, 2011 - IR 1297625; 0BOSR XFT

-A1, SH Area Heaters Testing Discrepancies, December 3, 2011

- Unit 2 Standing Order; Station Heat Coil Degradation in Unit 2 VA Plenum, Log #

11-053 - 0BOSR XFT-A1; Freezing Temperature Equipment Protection SH and Department Support Requirements, Revision 13

- 0BOSR XFT-A3; Freezing Temperature Equipment Protection Plant Ventilation Systems, Revision 8

- 0BOSR XFT-A4; Freezing Temperature Equipment Protection Area Buildings Ventilation Systems and Tanks, Revision 7

- 0BOSR XFT-A5; Freezing Temperature Equipment Protection Non

-Protected Area Buildings Ventilation Systems, Revision 6

4 Attachment

- BOP XFT-1; Cold Weather Operations, Revision 2

- IR 1298335; 0BOSR XFT

-A3 Freezing Temperature Protection Discrepancies, December 05, 2011 - Drawing M-62; Diagram of Residual Heat Removal, Revision BD

Section 1R04: Equipment Alignment (Quarterly)

- BAP 300-1A1; At The Controls Area, Revision 52

- BOP RH-E2A; Unit 2 Residual Heat Removal System Train A Electrical Lineup, Revision 4

- BOP RH-M2A; Unit 2 Residual Heat Removal System Train A Valve Lineup, Revision 10

- IR 0332862; 1B AF Pump Air Box Leakage, May 07, 2005

- IR 1289049; Fireproofing on Column Outside 1B AF Pump Room Degraded, November 10, 2011 - IR 1299293; AF005 Flow Control Valve Trim Clearance Low Margin Issue, November 21, 2011

IR 1304078; Fire Drill Observation

- SCBA Voice Amplifiers Not Working, December 17, 2011 - EC 355468; Evaluation of Diesel Driven Auxiliary Feedwater Air Box Gaps, Revision 0

- SPEC. L-2722 Proposed Seal for 2AB

-1086 Unit 2; Sheet Numbers 1A, 1, 2, and 3, Revision 1

- BOP AF-M2B; Auxiliary Feedwater Train B Valve Lineup, Revision 4

Section 1R04: Complete System Walkdown (Semi

-Annual)

- IR 1076490; Fire Damper 2VE04Y Access Door Hinge Tack Welds Broken, May 28, 2011

Section 1R05:

Fire Protection (Quarterly)

- IR 1075765; Electro

-Thermo-Link Separated, June 1, 2010

- IR 1077737;

Need CO2 OSS for 2 ICSRs on the T.S

. Fire Tamper Surveillance, June 7, 2010

- IR 1072592; 2VD23YA Flexible Conduit Support Clip not Holding Conduit, May 24, 2010

- IR 1072640; Debris in Tray Below Damper 2VD63Y, May 24, 2010

- IR 1073509; Flexible Conduit Loose

at Upper, South ETL on Fire Damper, May 26, 2010

- IR 1081618; Difficult to Access Damper, 1VE06Y for Surveillance/Repair, June 17, 2010

- IR 1289049; Fireproofing on Column Outside 1B AF Pump Room Degraded, November 10, 2011 - IR 1250346; Fire Brigade Leader Training Issue, August 12, 2011

- Fire Drill Scenario No. 11

-04; Unit 1 Auxiliary Boiler Room Fire, September

16, 2011 - Pre-Fire Plan; Fire Area/Zone

- FZ 8.3-1 Southeast, Revision 1

- EC 350613; Evaluation of Fire Damper S

-Hook Orientation Impact on Dampers 2VD24&B, VC191Y, and 0VC193Y, Revision 0

- WO 1197473; Tech Spec Fire Damper 18

-Month Visual Inspection, December

3, 2009 - WO 1028736; Tech Spec Fire Damper 18

-Month Visual Inspection, August 4, 2008

- WO 1124519; Tech Spec Fire Damper 18

-Month Visual Inspection, April 14, 2008

- WO 0848826; Tech Spec Fire Damper 18

-Month Visual Inspection, December 15, 2006

- 0BMSR 3.10.g.7; TRM Fire Damper 18

-Month Visual Inspection, Revision 13

- IR 1304076; Fire Drill Observation

- Personnel Walking Through SIM Smoke, December 17, 2011 - RM-AA-101; Records Management Program, Revision 9

- OP-AA-201-003; Fire Drill Performance, Revision 12

5 Attachment

Corrective Action Documents As a Result of NRC Inspection

IR 1291986; NRC Identified Fire Damper S

-Hook Orientation Issue, November

17, 2011 IR 1304063; NRC Identified Issues with S

-Hooks Not Resolved, December 17, 2011

- IR 1058790; Bad Fuse Found in 2RD06J Panel, April 20, 2011

Section 1R12:

Maintenance Effectiveness (Quarterly)

- IR 1061760; MG Set Motor Smoked on Attempted PM Start, April 26, 2011

- IR 1062164; Motor Cutoff Switch Replaced for 2RD 05E

-1B, April 27, 2011

- IR 1065922; Unit 2 Rods Will Not Manually Withdraw, May 5, 2010

- IR 1066455; Unit 2 RD07J Cabinet Capacitor Found Broken, May 6, 2011

- IR 1066490; 2A RD MG Set 1 OVT Timer Failed, May 6, 2011 - IR 1067031; Vibrations Levels on 2B Rod Drive MG Set Remain Unchanged, May 8, 2011

- IR 1290831; 1A RD MG Set Increased Vibrations, November 15, 2011

- BOP RD-5; Control Rod Drive MG Set Up and Paralleling to Operating Control Rod Drive MG Set, Revision

10 - ER-AA-600-1042; On-Line Risk Management, Revision 7

Section 1R13: Maintenance Risk Assessments and Emergent Work Control (Quarterly)

- ER-AA-600-1021; Risk Management Application Methodologies, Revision 4

- PC-AA-1014; Risk Management, Revision 2

- 0BOA ENV-1; Adverse Weather Conditions Unit 0, Rev. 108

- 1BOA ENV-1; Adverse Weather Conditions Unit 0, Rev. 102

- 0BOA ENV-2; Rock River Abnormal Water Level Unit 0, Rev. 100

- IR 1285254; Rock River Level Low, November 2, 2011

- IR 240597; Unplanned LOCAR Entry for 2A Emergency Diesel Generator Due to 2VD024YB Damper Section 1R15: Operability Evaluations (Quarterly)

- IR 240972; Fire Damper "S" Hook Installed Improperly, August 2, 2004

- IR 240985; Need Work Request for Fire Damper Inspections, August 2, 2004

- IR 248940; Fire Damper Issues Identified by NRC, August 31, 2004

- IR 249486; Fire Damper "S" Hook Issue Identified by NRC, September 2, 2004

- IR 297682; NRC Question About Fire Damper S

-Hooks, February 4, 2005

- IR 757875; Fire Damper S

-Hooks, April 1, 2008

- IR 1285361; Potential Multiple Starts of Diesel Driven AF Pump, November 2, 2011 - IR 1291986; NRC Identified Fire Damper S

-Hook Orientation Issue, November 17, 2011

- IR 1292337; Piping Between 2AF006B and 2AF017B Found Not Full, November 18, 2011

- IR 1295958; AF Improvement

Suggestion, November 18, 2011

- IR 1295958; AF Improvement Suggestion, November 18, 2011

- IR 1295488; EOC Review of Byron IP 1291986 Fire Damper S

-Hooks, November 29, 2011

- Three Mile Island Corrective Action Program Number TI999

-0943 linked to ETTS # 25169; One Section of Fire Damper AH

-FD-22 Did Not Close During Test, October 1, 1999

- EC 350613; Evaluation of Fire Damper S

-Hook Orientation Impact on Dampers 2VD24YB, VC191Y and OVC193Y, August 11, 2004

- EC 350550; Evaluation of Fire Damper S

-Hook Orientation Impact, August 31, 2004

- WO 1197473 01; Technical Specification Fire Damper 18 Month Visual Inspection, December 3, 2009

6 Attachment

- EC 383229; Fill Empty Pipe Between 1AF006A and 1AF017A, Close Drain Valve 1AF018A, and Throttle Open Vent Valve 1AF030A, Revision 0

- EC 383308; OP EVAL 11

-003, Small Voids in 2A and 2B SX to AF Suction Piping, Revision 0

- EC 386578; OP Evaluation 11

-009 Multiple Starts of Diesel AF Pump, November 8, 2011 - WO 1124519 01; Technical Specification Fire Damper 18 Month Visual Inspection,

April 14 , 2008 - WO 848828 01; Technical Specification Fire Damper 18 Month Visual Inspection, December 15, 2006 - BOP AF-3, Filling and Venting the Auxiliary Feedwater System, Revision 4

- M-1FW01147X; Drawing, Byron Unit 1 Support M

-1FW01147X, Rev. D

- M-1SI06010X; Drawing, Byron Unit 1 M

-1SI06010X Sub. E

- 13.1.29; Calculation for Mechanical Component Support M

-1SI06010X, Rev. D

- 13.1.29; Calculation for Mechanical Component Support M

-1SI06010X, Rev. E

- 13.1.29; Calculation for Mechanical Component Support M

-1SI06025V, Rev. F - 13.1.29-BYR97-359; 1SI06010X, 1SI06012X, 1SI06031X, 1SI06075X, 1SI06105X, and 1SI06155X. Evaluate Subsystem 1SI06 Supports for Additional Loads, Rev. 5

- 14.1.18-1FW01147; Calculation for Mechanical Component Support Number M

-1FW01147X, Rev. 0 - IR 1272187; Issues Applicable to Byron from Braidwood Mod/50.59 Inspection, October 4, 2011 - BRW-97-0827-M; Piping Evaluation for Lead Shielding on Subsystem 2SI06, Rev.

0 - RH-2; Large Bore Isometric, Residual Heat Removal System, Rev. 22

- IR 1276280; UFSAR Section 3.6 and Piping Design Specifications are Inconsistent, October 13, 2011 - IR 1276069; 1/2FW01 Piping Calculation Revisions Do Not Meet UFSAR Requirements, October 13, 2011 - IR 1272834; Incorrect Coding of Support Skew on 1FW01 Piping, October 5, 2011 - EMD-064195; Calculation, Addendum E to Piping Stress Report for Subsystem 1SI06, Rev.

5 - IR 1262559; BOP ID: Small Shift Trend in Major Plant Parameters, September 13, 2011 - IR 1265515; U1 RX Power Lowered Below 99.5% for LEFM Troubleshooting, September 16, 2011 - IR 1253439; LEFM Computer Point Is Off Normal Per 1BOSR CX

-M1, August 19, 2011

- IR 1263929; LEFM Alarms in IR 1241271 and Card Analysis

- OEM Review Results, September 16, 2011 - IR 1241271; LEFM Trouble Alarm

- Ramp Back, July 19, 2011

- IR 1241629; LEFM Trouble Alarm Causing Unit 1 Ramp Back Again, July 19, 2011

- IR 1277627; NRC Questions on HELB

- Presence of Openings, October 17, 2011

- IR 1279759; Added Scope to Turbine Building HELB Effort, October 21, 2011

- IR 1244251; HELB Discussion with the NRC Residents, July 26, 2011 - IR 1240295; Two New Line Break Locations Identified During HELB Analysis, July

15, 2011 - IR 1238611; Inoperability of ESF Components Due To HELB, July 11, 2011

- IR 1237133; Non

-Conservatism in Turbine Building HELB Analysis, July 6, 2011

- IR 1184258; Non-Conservatism in Turbine Building HELB Analysis, March 7, 2011

- IR 1276895; NRC Question

- Effect of Turbine Building HELB on Reactor Trip Breakers, October 14, 2011

- IR 1272802; 2B CS Pump Did Not Auto Start During 2B DG Sequence Test, October 5, 2011 Section 1R19: Post Maintenance Testing (Quarterly)

- WO 1476986 02; 2B CS Pump Did Not Auto Start During 2B DG Sequence Test, October 5, 2011

7 Attachment

- WO 1476986 03; 2B CS Pump Did Not Auto Start During 2B DG Sequence Test, October 5, 2011 - ER-AA-1200; Critical Component Failure Clock, Revision 7

- WO 1324847; 2AF014E IST Disassembly and Inspection, October 5, 2011

- WO 1324407; 2AF014G IST Disassembly and Inspection, October 5, 2011

- WO 1365478; 2AF014H IST Disassembly and Inspection, October 5, 2011

- 2BOSR 7.5.7

-2; Unit 2 Train B Auxiliary Feedwater Flow Path Operability Surveillance Following Shutdown, Rev. 6

- IR 1272927; 2B AF Static Pressure Gauge Indication Failed Low, October 5, 2011

- 2BOSR 0.5-2.RH.4-1; Unit 2 ASME Surveillance Requirements for Residual Heat Removal Pump Miniflow Valve 2RH610, Revision 5

Section 1R20:

Refueling and Other Outage Activities

- 2BGP 100-1; Plant Heatup, Revision 50

- 2BGP 100-2; Plant Startup, Revision 40

- 2BGP 100-3; Power Ascension, Revision 73

- IR 128875; Error in RCS Leakrate Data in MCR Logs, November 10, 2011

Section 1R22: Surveillance Testing (Quarterly)

- BOP AF-1; Diesel Driven Aux Feedwater Pump Alignment to Standby Condition, Revision 24

- BOP AF-7; Diesel Driven Auxiliary Feedwater Pump 1B Startup on Recirc, Revision 37

- BOP AF-7T1; Diesel Driven Auxiliary Feedwater Pump Operating Log, Revision 21

- BOP AF-8; Diesel Driven Auxiliary Feedwater Pump 1B Shutdown, Revision 22

- WO 1459476 01; 1AF01PB Group B IST Requirements for Diesel Driven AF Pump, October 28, 2011 - 1BOSR 7.5.4

-2; Unit 1 Diesel Driven Auxiliary Feedwater Pump Monthly Surveillance, Revision 14

- 2BOSR 8.1.11

-2; 2B Diesel Generator Sequencer Test 18 Month, Revision 11

- WO 1337989 01; 2B Diesel Generator Sequencer Test, October 5, 2011

- IR 1281160; 1SI8958B Failed Acceptance Criteria During 1B RH PP IST, October 25, 2011

- IR 1298289; Unit 2 RCS Leakrate Surveillance Needs Improvements, December 05, 2011

- 0BMSR FP-5; Fire Hydrant Yard Loop Annual Flush, Revision 8

- WO 1454082; 1RH01PB Group A IST Requirements for Residual Heat Removal Pump, October 25, 2011 - IR 1281160; 1SI8958B Failed Acceptance Criteria During 1B RH PP IST, October

25, 2011 Corrective Action Documents As a Result of NRC Inspection

- IR 1304054; Surveillance Improvements Needed, December 17, 2011

- AR 1214604; NOS ID B1R17 RP Outage Adverse Trend; 5/11/2011

2RS1: Radiological Hazard Assessment and Exposure Controls

(71124.01)

- AR 1243013; RP Response to Fire Alarm Did Not Meet Expectations; 7/22/2011

- AR 1248312; NOS ID Poor Contamination Boundary Controls in FHB;

8/5/2011 - BRP 5800-3; Area Radiation Monitoring System Alert/High Alarm Setpoints; Revision

25 - BRP 5820-14; Process Radiation Monitoring System Alert/High Alarm Setpoints; Revision 42

- RP-AA-460; Controls for High and Locked High Radiation Areas; Revision 2

0 - RP-AA-460-001; Controls for Very High Radiation Areas; Revision 2

8 Attachment

- RP-AA-460-003; Access to HRAs/LHRAs in Response to a Potential or Actual Emergency; Revision 1

- R P-AP-460; Access to Reactor In

-Core Sump Area; Revision 2

- Work Order 1094446 01; Non Accessible Charcoal Adsober Operability Test; 8/31/2009

2RS3: In-Plant Airborne Radioactivity Control and Mitigation

(71124.03)

- Work Order 1149597 01; Perform Recirc Charcoal Halide Test Control Room Ventilation System; 3/16/2010

- National Voluntary Laboratory Accreditation Program; Selected Records; Various Dates

2RS4: Occupational Dose Assessment (71124.04)

- AR 1106461; Non

-Conservative Liquid Discharge Alarm Setpoints; 8/26/2010

2RS5: Radiation Monitoring Instrumentation (71124.05)

- AR 1107149; Additional Investigation Required for ODCM/LCO Implementation; 8/29/2010

- AR 1302586; Non

-Conservative Setpoints Found for TRM Rad Monitors; 12/14/2011

- AR 1303888; Potential RETS Impact Due to Non

-Conservative PRM Setpoints; 12/16/2011

- BRP 5800-3; Area Radiation Monitoring System Alert/High Alarm Setpoints; Revision

25 - BRP 5820-12; Response to Area and Process Radiation Monitor LCOARS or Out of Service Conditions; Revision 28

- BRP 5820-14; Process Radiation Monitoring System Alert/High Alarm Setpoints; Revision 42

- BYR-10-001; Calculation of Liquid Process Radiation Monitor Set Points; 8/30/2010

- RP-BR-951; Set Point Changes for Process Radiation Monitors; ODCM (Effluent) Monitors; Revision 0.

- 2009 Byron Station Annual Radioactive Effluent Release Report; April 30, 2010

2RS6: Radioactive Gaseous and Liquid Effluent Treatment (71124.06) - 2010 Byron Station Annual Radioactive Effluent Release Report; April 29, 2011

- AR 00978684; Effluent Monitor Surveillance Not Performed Per Procedure; dated October 13, 20 09 - AR 00996917; Effluent Release Process

- Potential Gaps; dated November 22, 2009

- AR 01106461; Non

-Conservative Liquid Discharge Alarm Setpoints; dated August 26, 2010

- AR 01107146; Additional Investigation Required for ODCM/LCO Implementation; dated August 29, 2010

- AR 01108146; Treatment of Ar

-41 in Gaseous Effluents; dated August 31, 2010

- AR 1247902; 1/2 RE

-PR-028 Particulate Filters Could Not Be Located; 8/4/2011

- BCP-400-TWX01; Liquid Radwaste Release from Release Tank OWX01T; Revision

59 - CY-AA-120-400; Closed Cooling Water Chemistry; Revision 13

- CY-AA-120-420; Auxiliary Boiler Chemistry; Revision 10

- CY-AA-130-201; Radiochemistry Quality Control; Revision 1

- CY-AA-170-000; Radioactive Effluent and Environmental Monitoring Programs; Revision 5

- CY-BY-170-301; Offsite Dose Calculation Manual; Revision 6

- CY-BY-170-301; Offsite Dose Calculation Manual; Revision 7

- FASA 1013272; Radioactive Gaseous and Liquid Effluents (RETS); 9/17/2010

- FASA 831375; Radioactive Gaseous and Liquid Effluents (RETS); 3/31/2009

- Gaseous Discharge Permit Number 110411; dated October 13, 2011

- Gaseous Discharge Permit Number 110445; dated October 31, 2011

9 Attachment

- Liquid Discharge Permit Number 110437; dated October 25, 2011

- RP-BY-900-1PR29J; 1PR29J Process Radiation Monitor Radiological Air Sampling;

Revision 2 - RP-BY-900-2PR29J; 2PR29J Process Radiation Monitor Radiological Air Sampling; Revision 2 - Work Order 1110220 01; Fuel Handling Building Exhaust Charcoal Adsorber Bank Operability Test; 12/21/2009

- Work Order 1236016 01; Perform Calibration of Rad Monitor 1PR28J; 1/18/2011

- Work Order 1249358 01; Perform Surveillance Test of 2PR28J; 4/26/2011

- 2009 Byron Station Annual Radiological Environmental Operating Report; May 2010

2RS7: Radiological Environmental Monitoring Program (71124.07)

- 2010 Byron Station Annual Radiological Environmental Operating Report; May 2011

- 2010 Land Use Census; dated August 30, 2010

- AR 00958298; ODCM Vent Stack Coordinates Inaccurate; dated August 27, 2009

- AR 01034880; REMP Milk Sample

- Invalid Result; dated February

24, 2010 - AR 01090911; REMP Groundwater Sample Location No Longer Participating; dated July 15, 2010 - AR 01122156; REMP Sample Results above Detection Limit; dated October 5, 2010

- AR 01129610; Check

-In Self-Assessment on the Radiological Environmental Monitoring Program (REMP); Approved June 20, 2011

- AR 01223226; REMP Air Samples

- Positive Detects for I

-131; dated June 1, 2011

- Environmental, Inc. Sampling Manual, Revision 13

- AR 1015646; Non

-Conforming Waste Found in Radwaste Shipment; 1/12/2010

2RS8: Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and Transportation (71124.08)

- AR 1067394; Non

-Conforming Radioactive Waste in Shipment; 5/10/2010

- AR 1173307; RWS 10

-013 Contained Unapproved Mixed Waste; 2/10/2011

- AR 1221229; RWS11-006 Contained Un

-Manifested Asbestos; 5/26/2011

- AR 1231158; RWS 11

-001 Manifested for Material Not Present; 6/21/2011

- AR 1233858; NOS ID: Cause of IR Incorrect RW Shipping Paperwork Not Identified; 6/28/2011 - AR 1250262; NOS ID: RP Failed to Address NOS Issues

- Finding; 8/11/2011

- AR 1270337; Sea/Land Inventory Not Documented in Accordance with T&RM; 9/30/2011

- AR 1285148; QHPI Request for RP

- RWS Manifest; 11/2/2011

- AR 1285591; NRC Identified: DAW Container Inspections Outside of Procedure Guidance;

11/3/2011 - AR 928393928393 Non

-Conforming Metal Shipped to Bear Creek Processing; 6/5/2009

- Course Code N

-RPCTAR; DBIG RAM Shipping/Inspection; Revision 0

- FASA 9866572

-03; Radioactive Solid Waste Processing and Radioactive Material Handling, Storage and Transportation; 4/26/2011

- Letter BYRON

-2008-0123; Report of Changes, Tests, and Experiments; 12/12/2008

- Letter BYRON

-2010-0147; Report of Changes, Tests, and Experiments; 12/13/2010

- Module/LP ID RPTI 8.05; Radioactive Material Shipments; Revision 18

- NOSA-BYR-10-04 (AR 969170969170; Chemistry, Radwaste, Effluent and Environmental Monitoring Audit Report; 6/2/2010

- NOSA-BYR-11-06 (AR 1130876); Radiation Protection; 8/18/2011

10 Attachment

- Performance Training and Evaluation; Task 509

-004; Provide Radiological Protection Coverage During the Preparation of a Shipment of Radioactive Material; 11/5/2009

- Performance Training and Evaluation; Task 509

-010; Perform Surveys on Radioactive Material Transport Vehicles; date not provided

- Performance Training and Evaluation; Task 509

-013; Receipt Survey of Radioactive Material

- Radiation Protection Technician/Continuing Training; DBIG
Waste Acceptance Guidelines; Revision 0

- RP-AA-100; Process Control Program for Radioactive Wastes; Revision 7

- RP-AA-600; Radioactive Material/Waste Shipments; Revision

12 - RP-AA-600-1001; Exclusive Use and Emergency Response Information; Revision 6

- RP-AA-600-1003; Radioactive Waste Shipments to Barnwell and Defense Consolidation Facility (DCF); Revision 7

- RP-AA-600-1004; Radioactive Waste Shipments to Energy Solutions' Clive Utah Disposal Site Containerized Waste Facility; Revision 9

- RP-AA-600-1005; Radioactive Material and Non Disposal Site Waste Shipments; Revision 12

- RP-AA-601; Surveying Radioactive Material Shipments; Revision 13

- RP-AA-605 Attachment 1; Trending for Shifts in Scaling Factors; 01/20/2011

- RP-AA-605 Attachment 1; Trending for Shifts in Scaling Factors; 06/02/2011

- RP-AA-605 Attachment 1; Trending for Shifts in Scaling Factors; 10/03/2009

- RP-AA-605 Attachment 1; Trending for Shifts in Scaling Factors; 10/19/2010 - RP-AA-605 Attachment 1; Trending for Shifts in Scaling Factors; 2/17/2010

- RP-AA-605 Attachment 1; Trending for Shifts in Scaling Factors; 8/18/2010

- RP-AA-605 Attachment 1; Trending for Shifts in Scaling Factors; 9/16/2011

- RP-AA-605 Attachment 2; Waste Stream Results Review; DAW; 1/20/2011

- RP-AA-605 Attachment 2; Waste Stream Results Review; DAW; 3/30/2011

- RP-AA-605 Attachment 2; Waste Stream Results Review; DAW; 4/18/2010

- RP-AA-605 Attachment 2; Waste Stream Results Review; Primary Resin; 3/10/201

0 - RP-AA-605 Attachment 2; Waste Stream Results Review; Secondary Radwaste Filter; 4/24/2010 - RP-AA-605 Attachment 2; Waste Stream Results Review; Secondary Resin; 3/25/2010

- RP-AA-605; 10 CFR Part 61 Program; Revision 4

- Shipment RMS09

-094; Rx Vessel Dosimetry; Type A Package; 11/18/2009

- Shipment RMS11

-078; Dirty Laundry; Low Specific Activity (LSA

-II); 4/27/2011

- Shipment RWS10

-011; Dewatered Bead Resin; Low Specific Activity (LSA

-II); 6/29/2010

- Shipment RWS10

-012; DAW Trash; Low Specific Activity (LSA

-II); 9/1/2010 - Shipment RWS10

-013; DAW Trash and TR Pond Sludge; Low Specific Activity (LSA

-II); 9/1/2010 - IR 1139610; Potential Non

-Conservative Tech Specs for Component Cooling;

November 12, 2010 Section 4OA1: Performance Indicator Verification (71151)

- IR 1139728; CC System OLR Impact From IR 1139610;

November 12, 2010

- IR 1141591; 2A DG Emergency Stopped Due to Oil Leak;

November 17, 2010

- IR 1158910; RH System Issue Resulting in LER

- Tracking; January 05, 2011

- IR 1128409; Threshold for SSFF Approaching White Region; June 14, 2011

- IR 1284054; Legacy Issues with Main Steam Tunnel Pressurization Calculation;

October 31, 2011 - LS-AA-2080; NRC Safety System Functional Failure

- July 2010 to July 2011, Revision 4

- EC 382262; Byron OpEval #

10-006 - U-0 CC Pump Potential N

on-Conservative Tech Spec

11 Attachment

- LER 454/2010

-001; Technical Specifications Allowed Outage Time Extension Request for Component Cooling System Contained

Inaccurate Design Information that Significantly Impacted the Technical Justification, November 12, 2010

- LER 454/2011-001; Potential Loss of Residual Heat Removal System Safety Function in Mode 4 When Aligned for Shutdown Cooling Due to Potential for Flashing or Voiding of Coolant During a Shutdown Loss of Cooling Accident, January 5, 2011

- LER 455/2011

-001; Unit 2

Emergency Diesel Generator Inoperable for Longer than Allowed by Technical Specifications Due to Inadequate Work, November 17, 2011

- NEI 99-02 Revision 6; Regulatory Assessment Performance Indicator Guideline, October 2009

- Reactor Oversight Program MSPI Basis Document Revision 3; December 2006

- Monthly Data Elements for NRC Reactor Coolant System (RCS) Specific Activity, October

2010 - September 2011

- PWR High Pressure Safety Injection Function, October 2010

- September 2011

- Residual Heat Removal Function, October 2010

- September 2011

- PWR Auxiliary Feedwater/Emergency Feedwater Function, October 2010

- September 2011

- Cooling Water Support Function, October 2010

- September 2011

- IR 1154673; Unable to Perform Manual Stroke Surveillance of 1SX150A, December 20, 2010 - IR 1152376; Unit 2 CWS MSPI Exelon At

-Risk, December 14, 2010

- IR 1263487; CWS2 (SX) MSPI Low Margin, September 15, 2011

- IR 1090691; Unit 1 CWS MSPI At

-Risk, July 14, 2010

- Monthly Data Elements for NRC Unplanned Power Changes Per 7000 Critical Hours, June 2010 - October 2011

- IR 1259684; Byron PI in Variance

- P.8.1.2 Unplanned Power Changes, September 6, 2011

- IR 1116305; Runback of Byron Station U

-1 Due to 1A FW PP Trip, September 22, 2010

- IR 1271650; Difference Between Byron & Braidwood PPC Point Calcs Y2021 & Y2022

Section 4OA2: Identification and Resolution of Problems (7115

2) - IR 1282689; Pin Hole Leak in Area 7 on 2RY8028 P

-44 - IR 1289655; IR Indicates DG Fire Pump Started in Over Ride for Test CCP,

November 04, 2011 - 2BwOSR 3.8.1.14

-2; 2B DG 24 Hour Endurance Run, Revision 5

- WO 1323726; 2B DG 24 Hour Endurance Run 18 Month, September

13, 2011 - Analysis BYR11

-036; Turbine Building HELB and Room Heat Up Analyses for MUR PU, Revision 0

- EC 383599; Op Eval 11

-005, Turbine Building HELB Analysis Input Errors, Revision 1

- OWA Board Meeting Minutes; Year 2010 Quarter 4, December 28, 2010

- OWA Board Meeting Minutes; Year 2011 Quarter 1, April 5, 2011

- OWA Board Meeting Minutes; Year 2011 Quarter 2, June 30, 2011

- OWA Board Meeting Minutes; Year 2011 Quarter 3, October 14, 2011

- OWA Related IRs; 4Q2010

- 3Q2011 - IR 806396; Both Units SD Systems Degraded for >5 Years, August 12, 2008

- IR 1007239; Review SJAE Strainer Plugging for OWA/OC, December 18, 2009

- IR 1106359; Common Cause

- Recommend Venting SD During Stroke Time Surveillance, August 26, 2010

- IR 1118055; 2A Main Feed Pump Recirc Not Modulating Properly, September 26, 2010

- IR 1122751; Missed Fire Watches in the Past, October 06, 2010

- IR 1151298; Unit 1 Tower Overflow, December 12, 2010

- IR 1155725; Caustic Dilution Flow Only Reading 6 GPM, December 24, 2010

- IR 1158940; Multiple Failure of Employee Alarm System, January 1, 2011 - IR 1169182; MMD Support for 2B FW Pump Turning Gear Operation, January 31, 2011

12 Attachment

- IR 1172246; 0CW278A, Through Wall Crack on Valve Body, February 08, 2011

- IR 1172509; 0CW220 Flow Control Valve Not Repositioning Upon Demand, February 08, 2011 - IR 1194212; Operator Work Around, March 29, 2011

- IR 1194754; RSH CO2 TK Repair(s) Need to Be Expedited, March 30, 2011

- IR 1194754; Missed Closure of ATI, January 09, 2004

- IR 1211839; 2WG046 Drip Pan is Removed Consider Operator Challenge, May 4, 2011 - IR 1212344; Degradation of RSH CO2 Worsens, May 5, 2011 - IR 1216461; 2B CW PP Intake DP 9" Jumped to 2', May 16, 2011

Corrective Action Documents As a Result of

NRC Inspection

- IR 1276895; NRC Question

- Effect of TB HELB on Reactor Trip Breakers, October 14, 2011

- IR 1278980; NRC Question

- Maintaining VCT Pressure High for Chemistry, October

18, 2011 - EP-AA-1002; Exelon Nuclear Radiological Emergency Plan Annex for Byron Station; Revisions 26, 27, and 28

Section 1EP4

Emergency Action Level and Emergency Plan Changes - EP-AA-120-1001; 50.54(q) Program Evaluation and Effectiveness Reviews for Revisions

27 and 28 - EP-AA-120-F-01; EP Document Approval Forms for Revisions 27 and 28

13 Attachment

LIST OF ACRONYMS USE

D ADAMS Agencywide Document Access Management System

AF Auxiliary Feedwater

ALARA As-Low-As-Is-Reasonably

-Achievable

ANSI American National Standards Institute

ASME American Society of Mechanical Engineers CAP Corrective Action Program

CFR Code of Federal Regulations

CLB Current Licensing Basis

DAW Dry Active Waste

DG Emergency Diesel Generator

DOT Department of Transportation

EAL Emergency Action Level

ESF Engineered Safety Feature

HELB High Energy Line Break

HVAC Heating, Ventilation, and Air Conditioning

IMC Inspection Manual Chapter

IP Inspection Procedure

IR Inspection Report

IR Issue Report

IST Inservice Testing

LER Licensee Event Report

LORT Licensed Operator Requalification Training

MEE R Miscellaneous Electrical Equipment Room

MG Motor Generator

NEI Nuclear Energy Institute

OBE Operating Basis Earthquake

ODCM Offsite Dose Calculation Manual

OOS Out of Service

OpEval Operability Evaluation

OSP Outage Safety Plan

OWA Operator Workaround

ps ig pound per square inch gauge

MSPI Mitigating Systems Performance Index

NCV Non-Cited Violation

NRC U.S. Nuclear Regulatory Commission

NVLAP National Voluntary Laboratory Accreditation Program

PI Performance Indicator

RCS Reactor Coolant System

RFO Refueling Outage

RHR Residual Heat Removal

RWST Refueling Water Storage Tank

SDP Significance Determination Process

SH Station Heating

SRP Standard Review Plan

SSC Structure, System, and Component

SX Essential Service Water

TLD Thermoluminescent Detector

TS Technical Specification

14 Attachment

UFSAR Updated Final Safety Analysis Report

UL Underwriters Laboratory

URI Unresolved Item

VA Auxiliary Building Ventilation

WO Work Order

M. Pacilio

-2- In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document syste

m (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading

-rm/adams.html

(the Public Electronic Reading Room).

Sincerely, /RA/ Eric R. Duncan, Chie f Branch 3 Division of Reactor Projects Docket Nos. 50

-454; 50-455 License Nos. NPF

-37; NPF-66 Enclosure:

Inspection Report No. 05000454/

2011005 and 05000455/

2011005 w/Attachment: Supplemental Information

cc w/encl:

Distribution via ListServ

DOCUMENT NAME:

G:\DRPIII\BYRO\Byron 2011 005.docx

Publicly Available

Non-Publicly Available

Sensitive Non-Sensitive To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy

OFFICE RIII NAME EDuncan:dtp

DATE 02/07/12 OFFICIAL RECORD COPY

Letter to M. Pacilio from E. Duncan dated February 7, 2012.

SUBJECT: BYRON STATION, UNITS

1 AND 2, NRC INTEGRATED INSPECTION REPORT 05000454/2011005; 05000455/2011005

DISTRIBUTION:

Breeda Reilly

RidsNrrDorlLpl3

-2 Resource

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Jennifer Uhle

Steven Orth

Jared Heck

Allan Barker

Carole Ariano

Linda Linn

DRPIII DRSIII Patricia Buckley

Tammy Tomczak

ROPreports.Resource@nrc.gov