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| I ATTACHMENT A 4 DESCRIPTION AND SAFETY ANALYSIS OF PROPOSED CHANGES TO APPENDIX A TECHNICAL SPECIFICATIONS OF FACILITY OPERATING LICENSES FPF-37, NPF-66, NPF-72, AND NPF-77 A. DESCRIPTION OF THE PROPOSED CHANGE (SUPPLEMENTAL INFORMATION By letter dated January 30,1997, Commonwealth Edison (Comed) proposed to revise Technical Specifications (TS) 1.0, " Definitions," 3/4.6.1, " Primary Containment" and associated Bases, and 5.4.2," Reactor Coolant System Volume," for Byron Nuclear Power Station (Byron) and Braidwood Nuclear Power Station (Braidwood) to support steam generator replacement. Additionally, several editorial changes were also proposed to improve clarity and consistency of the TS. Comed will be replacing the original Westinghouse D4 steam generators (OSGs) at Byron and Braidwood with Babcock and Wilcox Intemational (BWI) steam generators. The replacement steam generators (RSGs) increase the Reactor Coolant System (RCS) volume which results in a higher calculated peak containment pressure (Pa ) value. Subsequent to the original submittal, issues penaining to the RCS volume have been raised which require that the original submittal be supplemented. The supplemental change affects only the RCS volume reported in TS Section 5.4.2. | | I ATTACHMENT A 4 DESCRIPTION AND SAFETY ANALYSIS OF PROPOSED CHANGES TO APPENDIX A TECHNICAL SPECIFICATIONS OF FACILITY OPERATING LICENSES FPF-37, NPF-66, NPF-72, AND NPF-77 A. DESCRIPTION OF THE PROPOSED CHANGE (SUPPLEMENTAL INFORMATION By {{letter dated|date=January 30, 1997|text=letter dated January 30,1997}}, Commonwealth Edison (Comed) proposed to revise Technical Specifications (TS) 1.0, " Definitions," 3/4.6.1, " Primary Containment" and associated Bases, and 5.4.2," Reactor Coolant System Volume," for Byron Nuclear Power Station (Byron) and Braidwood Nuclear Power Station (Braidwood) to support steam generator replacement. Additionally, several editorial changes were also proposed to improve clarity and consistency of the TS. Comed will be replacing the original Westinghouse D4 steam generators (OSGs) at Byron and Braidwood with Babcock and Wilcox Intemational (BWI) steam generators. The replacement steam generators (RSGs) increase the Reactor Coolant System (RCS) volume which results in a higher calculated peak containment pressure (Pa ) value. Subsequent to the original submittal, issues penaining to the RCS volume have been raised which require that the original submittal be supplemented. The supplemental change affects only the RCS volume reported in TS Section 5.4.2. |
| The proposed changes associated with this supplement are discussed in detail in Section E of this attachment. Affected TS pages showing the proposed volume changes for this supplement are included in Attachments B-1 and B-2 for Byron and Braidwood, resnectively. Improved Technical Specifications (ITS) are unaffected by this supplement since the value for RCS volume is not retained in ITS. | | The proposed changes associated with this supplement are discussed in detail in Section E of this attachment. Affected TS pages showing the proposed volume changes for this supplement are included in Attachments B-1 and B-2 for Byron and Braidwood, resnectively. Improved Technical Specifications (ITS) are unaffected by this supplement since the value for RCS volume is not retained in ITS. |
| B. DESCRIPTION OF THE CURRENT REQUIREMENT The description of the current TS requirements remains unchanged from the .~anuary 30, 1997 submittal. Only the section pertaining to this supplement is provided here for reference. | | B. DESCRIPTION OF THE CURRENT REQUIREMENT The description of the current TS requirements remains unchanged from the .~anuary 30, 1997 submittal. Only the section pertaining to this supplement is provided here for reference. |
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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217P6171999-10-21021 October 1999 Forwards non-proprietary & Proprietary Versions of HI-982083, Licensing Rept for Byron & Braidwood Nuclear Stations. Proprietary Rept Withheld,Per 10CFR2.790(b)(4) ML20217M2871999-10-21021 October 1999 Refers to Rev 5 Submitted in May 1999 for Portions of Byron Nuclear Power Station Generating Stations Emergency Plan Site Annex.Informs That NRC Approval Not Required Based on Determination That Plan Effectiveness Not Decreased ML20217M4361999-10-19019 October 1999 Forwards Rev 46 to Braidwood Station Security Plan, IAW 10CFR50.4(b)(4).Description of Changes,Listed.Encl Withheld Per 10CFR73.21 ML20217H4661999-10-18018 October 1999 Forwards Changes to EPIPs IAW 10CFR50.54(q) & 10CFR50,App E, Section V.Details of Changes Encl ML20217G9791999-10-14014 October 1999 Forwards SE Accepting Relief Requests to Rev 5 of First 10-year Interval Inservice Insp Program for Plant,Units 1 & 2 ML20217F7891999-10-0808 October 1999 Forwards Insp Repts 50-454/99-12 & 50-455/99-12 on 990803- 0916.One Violation Occurred Being Treated as NCV ML20217B6351999-10-0505 October 1999 Forwards for Info,Final Accident Sequence Precursor Analysis of Operational Event at Byron Station,Unit 1,reported in LER 454/98-018 & NRC Responses to Util Specific Comments Provided in ML20212L1791999-10-0505 October 1999 Informs That as Result of Staff Review of Util Responses to GL 92-01,rev 1,suppl 1 & Suppl 1 Rai,Staff Revised Info in Rvid & Is Releasing Rvid Version 2 ML20217B2991999-10-0101 October 1999 Forwards Insp Repts 50-454/99-16 & 50-455/99-16 on 990907-10.No Violations Noted.Water Chemisty Program Was Well Implemented,Resulted in Effective Control of Plant Water Chemistry ML20216J8241999-09-30030 September 1999 Notifies of Removal of NRC Headquarters & Region III Offices from Controlled Copy Distribution of Certain CE Documents. Specific Documents,Associated Controlled Copy Numbers & NRC Location Affected Are Shown on Attachment to Ltr ML20212J6751999-09-30030 September 1999 Forwards Replacement Pages Eight Through Eleven of Insp Repts 50-454/99-15 & 50-455/99-15.Several Inaccuracies with Docket Numbers & Tracking Numbers Occurred in Repts ML20217A5821999-09-29029 September 1999 Advises of NRC Plans for Future Insp Activities at Facility for Licensee to Have Opportunity to Prepare for Insps & to Provide NRC with Feedback on Any Planned Insps Which May Conflict with Plant Activities ML20217A9311999-09-29029 September 1999 Informs That NRC 6-month Review of Braidwood Identified That Performance in Maint Area Warranted Increased NRC Attention. Addl Insps Beyond Core Insp Program Will Be Conducted Over Next 6 Months to Better Understand Causes of Problem ML20216H4301999-09-23023 September 1999 Informs That Arrangements Made for Administration of Licensing re-take Exams at Braidwood Generating Station for Week of 991108 ML20216F7441999-09-17017 September 1999 Forwards Insp Repts 50-456/99-13 & 50-457/99-13 on 990706-0824.Three Violations Noted & Being Treated as Ncvs. Insp Focused on C/As & Activities Addressing Technical Concerns Identified During Design Insp Completed on 980424 ML20216F8051999-09-17017 September 1999 Forwards Insp Rept 50-454/99-14 & 50-455/99-14 on 990823-27. Security Program Was Effectively Implemented in Areas Inspected.No Violations Were Identified ML20212A6991999-09-10010 September 1999 Forwards SE Accepting Licensee Second 10-year Interval ISI Program Request for Relief 12R-07 for Plant,Units 1 & 2 ML20211Q9011999-09-0808 September 1999 Advises That Us Postal Service Mailing Address Has Changed for Braidwood Station.New Address Listed ML20211P1841999-09-0808 September 1999 Forwards Insp Repts 50-454/99-15 & 50-455/99-15 on 990824- 26.No Violations Noted.Objective of Insp to Determine Whether Byron Nuclear Generating Station Emergency Plan Adequate & If Emergency Plan Properly Implemented ML20211Q6821999-09-0606 September 1999 Informs That NRC Tentatively Scheduled Initial Licensing Exam for Byron Operator Licesne Applicants During Wks of 000619 & 26.Validation of Exam Will Occur at Station During Wk of 000529 ML20211Q6611999-09-0606 September 1999 Informs That NRC Tentatively Scheduled Initial Licensing Exam for Braidwood Operator License Applicants During Wk of 010115 & 22.Validation of Exam Will Occur at Station During Wk of 001218 ML20211P1901999-09-0303 September 1999 Forwards Insp Repts 50-456/99-12 & 50-457/99-12 on 990707-0816.No Violations Noted.Insp Generally Characterized by safety-conscious Operations,Sound Engineering & Maint Practices & Careful Radiological Work Controls ML20211N5151999-09-0303 September 1999 Ack Receipt of Re Safety Culture & Overtime Practices at Byron Nuclear Power Station.Copy of Recent Ltr from NRC to Commonwealth Edison Re Overtime Practices & Safety Culture Being Provided ML20211K1081999-09-0202 September 1999 Responds to Request for Addl Info to GL 92-01,Rev 1,Suppl 1, Reactor Vessel Structural Integrity, for Braidwood,Units 1 & 2 & Byron,Unit 2 ML20211M1371999-09-0202 September 1999 Discusses 990527 Meeting with Ceco & Byron Station Mgt Re Overtime Practices & Conduciveness of Work Environ to Raising Safety Concerns at Byron Station.Insp Rept Assigned for NRC Tracking Purposes.No Insp Rept Encl ML20211P1761999-09-0202 September 1999 Discusses Licensee Aug 1998 Rev 3K to Portions of Braidwood Nuclear Power Station Generating Stations Emergency Plan Site Annex Submitted Under Provisions of 10CFR50.54(q). NRC Approval Not Required ML20211G1221999-08-27027 August 1999 Forwards fitness-for-duty Program Performance Data for Each of Comm Ed Nuclear Power Stations & Corporate Support Employees within Scope of Rule for six-month Period Ending 990630,IAW 10CFR26.71(d) ML20211G4021999-08-25025 August 1999 Forwards Insp Repts 50-454/99-10 & 50-455/99-10 on 990622-0802.No Violations Noted ML20211B8691999-08-20020 August 1999 Forwards Insp Repts 50-254/99-10,50-265/99-10,50-454/99-09, 50-455/99-09,50-456/99-10 & 50-457/99-10 on 990628-0721. Action Plans Developed to Address Configuration Control Weaknesses Not Totally Effective as Listed BW990053, Forwards post-outage Summary Rept for ISI Examinations Conducted During Seventh Refueling Outage of Braidwood Station,Unit 21999-08-13013 August 1999 Forwards post-outage Summary Rept for ISI Examinations Conducted During Seventh Refueling Outage of Braidwood Station,Unit 2 BW990052, Informs That RW Clay,License OP-31044,no Longer Requires Operator License at Braidwood Station1999-08-12012 August 1999 Informs That RW Clay,License OP-31044,no Longer Requires Operator License at Braidwood Station 05000454/LER-1998-008, Informs That Licensee Determined That Suppl Rept to LER 98-008 Is Not Warranted.No Addl Info Was Generated Following Completion of Root Cause Investigation of Following Completion of Corrective Actions Stated in Original LER1999-08-12012 August 1999 Informs That Licensee Determined That Suppl Rept to LER 98-008 Is Not Warranted.No Addl Info Was Generated Following Completion of Root Cause Investigation of Following Completion of Corrective Actions Stated in Original LER ML20210N5651999-08-0606 August 1999 Forwards Rev 8 to Nuclear Generating Stations Emergency Plan, for Plants.With Summary of Changes ML20210U8031999-08-0404 August 1999 Forwards SER Granting Licensee Relief Requests VR-1,VR-3 & Portion of VR-2 Pursuant to 10CFR50.55a(a)(3)(ii).Relief Request VR-4 Does Not Require Explicit NRC Approval for Second 10-year Inservice Testing Program BW990049, Informs NRC of Plans to Demonstrate Compliance with 10CFR50.46 Requirements for Fuel Predicted to Experience Fuel Pellet to Rod Cladding Gap Reopening,During Current Cycle1999-08-0404 August 1999 Informs NRC of Plans to Demonstrate Compliance with 10CFR50.46 Requirements for Fuel Predicted to Experience Fuel Pellet to Rod Cladding Gap Reopening,During Current Cycle ML20210M9131999-08-0202 August 1999 Forwards Response to NRC AL 99-02, Operating Reactor Licensing Action Estimates, for Fys 2000 & 2001 for Comed ML20210K0771999-07-30030 July 1999 Submits 30-day Rept Re Discovery of ECCS Evaluation Model Error for Byron & Braidwood Stations,As Required by 10CFR50.46 ML20210K9761999-07-30030 July 1999 Forwards SE Accepting Licensee 60-day Response to GL 96-05, Periodic Verification of Design Basis Capability of Safety-Related Movs, for Plant ML20210G6291999-07-29029 July 1999 Forwards Insp Repts 50-456/99-11 & 50-457/99-11 on 990525-0706.Two Violations Noted & Being Treated as NCV, Consistent with App C of Enforcement Policy ML20210J8951999-07-29029 July 1999 Submits Other Actions,As Described,To Be Taken for Valves to Resolve Potential Pressure Locking Concerns,In Light of Extended Period for Valve Bonnet Natural Depressurization,In Response to GL 95-07, Pressure Locking & Thermal.. BW990045, Forwards Errata to 1998 Radioactive Effluent Release Rept. Info Has Been Corrected & Revised Spreadsheets Included in Attachment to Ltr1999-07-28028 July 1999 Forwards Errata to 1998 Radioactive Effluent Release Rept. Info Has Been Corrected & Revised Spreadsheets Included in Attachment to Ltr ML20210E2151999-07-23023 July 1999 Forwards Byron Unit 1 B1R09 ISI Summary Rept Spring 1999 Outage,980309-990424, in Compliance with Requirements of Article IWA-6000, Records & Repts of Section XI of ASME & P&PV,1989 Edition ML20216D3781999-07-21021 July 1999 Forwards Revised NFM9900022, Braidwood Unit 2 Cycle 8 COLR on ITS Format & W(Z) Function, to Account for Error That W Discovered in Computer Code Used to Calculate PCT During LBLOCA ML20210C3961999-07-20020 July 1999 Forwards Insp Repts 50-456/99-09 & 50-457/99-09 on 990517-0623.No Violations Noted.Weakness Identified on 990523,when Station Supervisors Identified Individual Sleeping in Cable Tray in RCA ML20216D7061999-07-19019 July 1999 Forwards Rev 45 to Braidwood Station Security Plan,Iaw 10CFR50.4(b)(4).Plan Includes Listed Changes.Rev Withheld, Per 10CFR73.21 BW990042, Forwards Braidwood Station,Unit 1 Post Accident Monitoring Rept for Reactor Vessel Level Indication Sys (Rvlis),Due to Facility Train B RVLIS Being Restored to Operable Status After 7-day Completion Time,Per TS 3.3.3 & 5.6.71999-07-16016 July 1999 Forwards Braidwood Station,Unit 1 Post Accident Monitoring Rept for Reactor Vessel Level Indication Sys (Rvlis),Due to Facility Train B RVLIS Being Restored to Operable Status After 7-day Completion Time,Per TS 3.3.3 & 5.6.7 ML20209H2991999-07-16016 July 1999 Withdraws 980529 LAR to Credit Automatic PORV Operation for Mitigation of Inadvertent Safety Injection at Power Accident.Response to NRC 990513 RAI Re LAR Encl ML20210A3151999-07-16016 July 1999 Forwards Insp Repts 50-454/99-08 & 50-455/99-08 on 990511-0621.Three Violations Being Treated as Noncited Violations ML20210B7071999-07-16016 July 1999 Responds to Requesting Review & Approval of Three Proposed Changes to Ceco QA TR,CE-1A Per 10CFR50.54(a)(3) & 10CFR50.4(b)(7) BW990040, Forwards Revised Monthly Operating Repts for May 1999 for Braidwood Station,Units 1 & 2.Since Issuance of Rept,It Was Determined That Rt That Occurred on Unit 2 During Startup Was Inadvertently Omitted1999-07-15015 July 1999 Forwards Revised Monthly Operating Repts for May 1999 for Braidwood Station,Units 1 & 2.Since Issuance of Rept,It Was Determined That Rt That Occurred on Unit 2 During Startup Was Inadvertently Omitted 1999-09-08
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217P6171999-10-21021 October 1999 Forwards non-proprietary & Proprietary Versions of HI-982083, Licensing Rept for Byron & Braidwood Nuclear Stations. Proprietary Rept Withheld,Per 10CFR2.790(b)(4) ML20217M4361999-10-19019 October 1999 Forwards Rev 46 to Braidwood Station Security Plan, IAW 10CFR50.4(b)(4).Description of Changes,Listed.Encl Withheld Per 10CFR73.21 ML20217H4661999-10-18018 October 1999 Forwards Changes to EPIPs IAW 10CFR50.54(q) & 10CFR50,App E, Section V.Details of Changes Encl ML20216J8241999-09-30030 September 1999 Notifies of Removal of NRC Headquarters & Region III Offices from Controlled Copy Distribution of Certain CE Documents. Specific Documents,Associated Controlled Copy Numbers & NRC Location Affected Are Shown on Attachment to Ltr ML20211Q9011999-09-0808 September 1999 Advises That Us Postal Service Mailing Address Has Changed for Braidwood Station.New Address Listed ML20211G1221999-08-27027 August 1999 Forwards fitness-for-duty Program Performance Data for Each of Comm Ed Nuclear Power Stations & Corporate Support Employees within Scope of Rule for six-month Period Ending 990630,IAW 10CFR26.71(d) BW990053, Forwards post-outage Summary Rept for ISI Examinations Conducted During Seventh Refueling Outage of Braidwood Station,Unit 21999-08-13013 August 1999 Forwards post-outage Summary Rept for ISI Examinations Conducted During Seventh Refueling Outage of Braidwood Station,Unit 2 05000454/LER-1998-008, Informs That Licensee Determined That Suppl Rept to LER 98-008 Is Not Warranted.No Addl Info Was Generated Following Completion of Root Cause Investigation of Following Completion of Corrective Actions Stated in Original LER1999-08-12012 August 1999 Informs That Licensee Determined That Suppl Rept to LER 98-008 Is Not Warranted.No Addl Info Was Generated Following Completion of Root Cause Investigation of Following Completion of Corrective Actions Stated in Original LER BW990052, Informs That RW Clay,License OP-31044,no Longer Requires Operator License at Braidwood Station1999-08-12012 August 1999 Informs That RW Clay,License OP-31044,no Longer Requires Operator License at Braidwood Station ML20210N5651999-08-0606 August 1999 Forwards Rev 8 to Nuclear Generating Stations Emergency Plan, for Plants.With Summary of Changes BW990049, Informs NRC of Plans to Demonstrate Compliance with 10CFR50.46 Requirements for Fuel Predicted to Experience Fuel Pellet to Rod Cladding Gap Reopening,During Current Cycle1999-08-0404 August 1999 Informs NRC of Plans to Demonstrate Compliance with 10CFR50.46 Requirements for Fuel Predicted to Experience Fuel Pellet to Rod Cladding Gap Reopening,During Current Cycle ML20210M9131999-08-0202 August 1999 Forwards Response to NRC AL 99-02, Operating Reactor Licensing Action Estimates, for Fys 2000 & 2001 for Comed ML20210K0771999-07-30030 July 1999 Submits 30-day Rept Re Discovery of ECCS Evaluation Model Error for Byron & Braidwood Stations,As Required by 10CFR50.46 ML20210J8951999-07-29029 July 1999 Submits Other Actions,As Described,To Be Taken for Valves to Resolve Potential Pressure Locking Concerns,In Light of Extended Period for Valve Bonnet Natural Depressurization,In Response to GL 95-07, Pressure Locking & Thermal.. BW990045, Forwards Errata to 1998 Radioactive Effluent Release Rept. Info Has Been Corrected & Revised Spreadsheets Included in Attachment to Ltr1999-07-28028 July 1999 Forwards Errata to 1998 Radioactive Effluent Release Rept. Info Has Been Corrected & Revised Spreadsheets Included in Attachment to Ltr ML20210E2151999-07-23023 July 1999 Forwards Byron Unit 1 B1R09 ISI Summary Rept Spring 1999 Outage,980309-990424, in Compliance with Requirements of Article IWA-6000, Records & Repts of Section XI of ASME & P&PV,1989 Edition ML20216D3781999-07-21021 July 1999 Forwards Revised NFM9900022, Braidwood Unit 2 Cycle 8 COLR on ITS Format & W(Z) Function, to Account for Error That W Discovered in Computer Code Used to Calculate PCT During LBLOCA ML20216D7061999-07-19019 July 1999 Forwards Rev 45 to Braidwood Station Security Plan,Iaw 10CFR50.4(b)(4).Plan Includes Listed Changes.Rev Withheld, Per 10CFR73.21 ML20209H2991999-07-16016 July 1999 Withdraws 980529 LAR to Credit Automatic PORV Operation for Mitigation of Inadvertent Safety Injection at Power Accident.Response to NRC 990513 RAI Re LAR Encl BW990042, Forwards Braidwood Station,Unit 1 Post Accident Monitoring Rept for Reactor Vessel Level Indication Sys (Rvlis),Due to Facility Train B RVLIS Being Restored to Operable Status After 7-day Completion Time,Per TS 3.3.3 & 5.6.71999-07-16016 July 1999 Forwards Braidwood Station,Unit 1 Post Accident Monitoring Rept for Reactor Vessel Level Indication Sys (Rvlis),Due to Facility Train B RVLIS Being Restored to Operable Status After 7-day Completion Time,Per TS 3.3.3 & 5.6.7 BW990040, Forwards Revised Monthly Operating Repts for May 1999 for Braidwood Station,Units 1 & 2.Since Issuance of Rept,It Was Determined That Rt That Occurred on Unit 2 During Startup Was Inadvertently Omitted1999-07-15015 July 1999 Forwards Revised Monthly Operating Repts for May 1999 for Braidwood Station,Units 1 & 2.Since Issuance of Rept,It Was Determined That Rt That Occurred on Unit 2 During Startup Was Inadvertently Omitted ML20207H7501999-07-12012 July 1999 Forwards Revised Pressure Temp Limits Rept, for Byron Station,Units 1 & 2.Revised Pressurized Thermal Shock Evaluations,Surveillance Capsule Rept & Credibility Repts, Also Encl ML20209G1391999-07-0909 July 1999 Forwards Results of SG Tube Insps Performed During Byron Station,Unit 1,Cycle 9 Refueling Outage within 12 Months Following Completion of Insps ML20196J9061999-07-0101 July 1999 Provides Evidence That Util Maintains Guarantee of Payment of Deferred Premiums in Amount of $10 Million for Each of Thirteen Reactors,Per 10CFR140.21 ML20196J9131999-07-0101 July 1999 Submits Status of Nuclear Property Insurance Currently Maintained for Braidwood,Byron,Dresden,Lasalle County,Quad Cities & Zion Nuclear Power Stations,Per 10CFR50.54(w)(3) ML20209B8241999-06-30030 June 1999 Forwards Five 3.5 Inch Computer Diskettes Containing Revised Annual Dose Repts for 1994 Through 1998 for Individuals Receiving Neutron Dose Not Previously Included in Reported Total Effective Dose Equivalent Values.Without Diskettes ML20196G2161999-06-25025 June 1999 Forwards for NRC Region III Emergency Preparedness Inspector,Two Copies of Comed Emergency Preparedness Exercise Manual for 1999 Byron Station Annual Exercise. Exercise Is Scheduled for 990825.Without Encls ML20209D4861999-06-17017 June 1999 Informs That R Heinen,License OP-30953-1 & a Snow,License SOP-30212-3,no Longer Require License at Byron Station 05000456/LER-1998-004, Forwards LER 98-004-01,IAW 10CFR50.73(a)(2)(i)(B). LER 98-004 Included Commitment to Transmit Supplemental Rept by 990628,due to on-going Evaluations1999-06-16016 June 1999 Forwards LER 98-004-01,IAW 10CFR50.73(a)(2)(i)(B). LER 98-004 Included Commitment to Transmit Supplemental Rept by 990628,due to on-going Evaluations 05000457/LER-1998-003, Forwards LER 98-003-00 Re Unit 2 Reactor Trip.Actions & Associated Action Tracking Number That Braidwood Station Is Committed to Implement in Response to LER Described Below1999-06-16016 June 1999 Forwards LER 98-003-00 Re Unit 2 Reactor Trip.Actions & Associated Action Tracking Number That Braidwood Station Is Committed to Implement in Response to LER Described Below 05000456/LER-1999-001, Forwards LER 99-001-00,IAW 10CFR50.73(a)(2)(i)(B). Description of Action & Associated Action Request Number That Braidwood Station Is Committed to Implement Is Response to LER Is Listed1999-06-15015 June 1999 Forwards LER 99-001-00,IAW 10CFR50.73(a)(2)(i)(B). Description of Action & Associated Action Request Number That Braidwood Station Is Committed to Implement Is Response to LER Is Listed BW990028, Forwards Braidwood Unit 2 Cycle 8 COLR in ITS Format & W(Z) Function, IAW TS 5.6.51999-06-10010 June 1999 Forwards Braidwood Unit 2 Cycle 8 COLR in ITS Format & W(Z) Function, IAW TS 5.6.5 05000454/LER-1999-002, Forwards LER 99-002-00,IAW 10CFR50.73(a)(2)(i)(b).There Are Two Actions Remaining to Address Cause of Event.Both Actions Are Listed1999-06-0808 June 1999 Forwards LER 99-002-00,IAW 10CFR50.73(a)(2)(i)(b).There Are Two Actions Remaining to Address Cause of Event.Both Actions Are Listed ML20195E3451999-06-0707 June 1999 Forwards 3.5 Inch Computer Diskette Containing Revised File Format for Annual Dose Rept for 1998,per 990520 Telcon Request from Nrc.Each Station Data Is Preceded by Header Record,Which Provides Info Necessary to Identify Data ML20195D6351999-06-0404 June 1999 Notifies NRC of Actions That Has Been Taken in Accordance with 10CFR26, Fitness for Duty Programs ML20211M1611999-05-28028 May 1999 Discusses 990527 Meeting with Comed Re Safety Culture & Overtime Control at Byron Nuclear Plant from Videoconference Location at NRC Headquarters.Requests That Aggressive Actions Be Taken to Ensure That Comed Meets Expectations ML20207D5261999-05-26026 May 1999 Forwards Response to NRC 990318 RAI Concerning Alleged Chilling Effect at Byron Station.Attachment Contains Responses to NRC 12 Questions ML20195C7911999-05-25025 May 1999 Forwards Revised COLR for Byron Unit 2,IAW 10CFR50.59.Rev Accounts for Planned Increase of Reactor Coolant Full Power Average Operating Temp from 581 F to 583 F ML20211M1781999-05-25025 May 1999 Summarizes Concerns with Chilling Effect & Overtime Abuses at Commonwealth Edison,Byron Station.Request That Ltr Be Made Part of Permanent Record of 990527 Meeting 05000454/LER-1999-001, Forwards LER 99-001-00,IAW 10CFR50.73(a)(2)(i)(B).Required Actions to Address Causes of Event Listed1999-05-21021 May 1999 Forwards LER 99-001-00,IAW 10CFR50.73(a)(2)(i)(B).Required Actions to Address Causes of Event Listed 05000457/LER-1999-002, Forwards LER 99-002-00,IAW 10CFR50.73(a)(2)(iv).Commitments Made by Util Are Listed1999-05-21021 May 1999 Forwards LER 99-002-00,IAW 10CFR50.73(a)(2)(iv).Commitments Made by Util Are Listed ML20195B2301999-05-19019 May 1999 Requests Approval of Proposed Changes to QA Topical Rept CE-1-A,rev 66a.Attachment a Describes Changes,Reason for Change & Basis for Concluding That Revised QAP Incorporating Proposed Changes Continues to Satisfy 10CFR50AppB ML20207E9831999-05-18018 May 1999 Forwards Copy of Commonwealth Edison Co EP Exercise Evaluation Objectives for 1999 Byron Station Annual EP Exercise,Which Will Be Conducted on 990825.Without Encl ML20206T3351999-05-17017 May 1999 Provides Written follow-up of Request for NOED Re Extension of Shutdown Requirement of TS Limiting Condition for Operation 3.0.3.Page 9 of 9 of Incoming Submittal Not Included ML20206N7861999-05-14014 May 1999 Forwards 1998 Annual Radiological Environ Operating Rept for Braidwood Station. Rept Contains Info Associated with Stations Radiological Environ & Meteorological Monitoring Programs ML20206Q8521999-05-13013 May 1999 Submits Rept on Numbers of Tubes Plugged or Repaired During SG Inservice Insp Activities Conducted During Plant Seventh Refueling outage,A2R07,per TS 5.6.9 ML20206N8551999-05-11011 May 1999 Forwards 1998 Annual Radioactive Environ Operating Rept for Byron Station. Rept Includes Summary of Radiological Liquid & Gaseous Effluents & Solid Waste Released from Site ML20210C7221999-05-0303 May 1999 Forwards Initial License Exam Matls for Review & Approval. Exam Scheduled for Wk of 990607 ML20206F5381999-04-30030 April 1999 Forwards Magnetic Tape Containing Annual Dose Repts for 1998 for Braidwood,Byron,Dresden,Lasalle County,Quad Cities & Zion Nuclear Power Stations,Per 10CFR20.2206(c).Without Magnetic Tape ML20206U3351999-04-30030 April 1999 Forwards Evaluation of Matter Described in Re Byron Station.Concludes That Use of Overtime at Byron Station Was Controlled IAW Administrative Requirements & Mgt Expectations Established to Meet Overtime Requirement of TS 1999-09-08
[Table view] |
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Commonwealth Edrum Company j
- p llraidwmed Generating Station
- %, , . Route et. Iku H 6 tiraceville. IL 60607@619 Tel H15-45&2He1 December 9,'1997 United States Nuclear Regulatory Commission Washington, D.C. 20555 Attention: Document Control Desk
Subject:
Byron Nuclear Power Station, Units 1 & 2 Facility Operating Licenses NPF-37 & NPF-66 NRC Docket No. 50-454 and 50-455 Braidwood Nuclear Power Station, Units 1 & 2 Facility Operating Licenses NPF-72 & NPF-77 NBC Docket No. 50-456 and 50-451 Supplement to Technical Speification Amendment Pertaining to Primary Containment and Reactor Coolant System Volume -
References:
- 1. J. Hosmer (Comed) Letter to USNRC, Primary Containment and Reactor Coolant System Amendment, dated January 30,1997
- 2. USNRC Request for Additional Information legarding Primary Containment and Reactor Coolant System, dated March 20,1997
- 3. J. Hosmer (Comed) Letter to USNRC, Primary Containment and Reactor Coolant System RAI Response, dated May 23,1997
- 4. J. Hosmer (Comed) Letter to USNRC, Primary Containment and Reactor Coolant System RAI Response to Question M, dated August 8,1997
- 5. J. Hosmer (Comed) Letter to USNRC, Primary Containment and Reactor Coolant System Update to RAI Response, dated November 11,1997 In Reference 1, Comed submitted a request for a License Amendment in accordance with 10CFR50.90 regarding the revised calculated peak containment pressure, P., and the increased RCS volume. These changes are associated with ti.e replacement steam generators to be installed on Byror and Braidwood Units 1. Subsequent to that submittal, he NRC Staffissued a Request for Additional Information regarding the proposed change t Jeference 2). Comed responded to that request in References 3,4 and 5.
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p U.S. Nuclear Regulatory Commission December 9,1997 This supplement is needed due to an error diu: overed in the current technical ,
specifications with regards to total RCS volume and a correction to the increase in RCS volume associated with the Unit 1 Replacement Steam Generators (RSGs) accounting for hot conditions. These changes affect Unit I and Unit 2 at both Byron and Braidwood.
During the process of preparing this technical specification revision, Comed evaluated the validation of the accident analysis (Spurious Safety Injection) related to the reactor coolant volume change. A potential conflict between the UFSAR assumptions and the Emergency Operating Procedures (EOPs) was discovered. Specifically, the EOPs do not provide explicit direction for the manual action of the Power Operated Relief Valve (PORV) as stated in the FSAR. Comed will determine whether to revise the UFSAR to
, credit automatic actuation of the PORVs, or whether to revise EOPs to support manual action, and will inform the NRC cf the results of this determination by 12/19/97.
This determination will not change the content of the amendment request or the results of this supporting analysis.
Enclosed is:
Attachment A: Detailed Description of the Proposed Changes Attachmer.t B-1 A: Byron Marked-Up pages Attachment B-2A: Braidwood Marked-up pages
> Attachment C: Evaluation of Significant Hazards Consideration Attachment D: Environmental Assessment Please address any comments or questions regarding this information to this atlice.
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- Sincerely, l
+ S hw 8 John B. Hosmer Vice Preside <t cc: Regional Administrator-RIII Byron /Braidwood Project Manager - NRR Senior Resident Inspector- Byron Senior Resident Inspector - Braidwood -
OfIice of N.sclear Safety -IDNS Kadshttmdsyp/pwnwdoc2
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I ATTACHMENT A 4 DESCRIPTION AND SAFETY ANALYSIS OF PROPOSED CHANGES TO APPENDIX A TECHNICAL SPECIFICATIONS OF FACILITY OPERATING LICENSES FPF-37, NPF-66, NPF-72, AND NPF-77 A. DESCRIPTION OF THE PROPOSED CHANGE (SUPPLEMENTAL INFORMATION By letter dated January 30,1997, Commonwealth Edison (Comed) proposed to revise Technical Specifications (TS) 1.0, " Definitions," 3/4.6.1, " Primary Containment" and associated Bases, and 5.4.2," Reactor Coolant System Volume," for Byron Nuclear Power Station (Byron) and Braidwood Nuclear Power Station (Braidwood) to support steam generator replacement. Additionally, several editorial changes were also proposed to improve clarity and consistency of the TS. Comed will be replacing the original Westinghouse D4 steam generators (OSGs) at Byron and Braidwood with Babcock and Wilcox Intemational (BWI) steam generators. The replacement steam generators (RSGs) increase the Reactor Coolant System (RCS) volume which results in a higher calculated peak containment pressure (Pa ) value. Subsequent to the original submittal, issues penaining to the RCS volume have been raised which require that the original submittal be supplemented. The supplemental change affects only the RCS volume reported in TS Section 5.4.2.
The proposed changes associated with this supplement are discussed in detail in Section E of this attachment. Affected TS pages showing the proposed volume changes for this supplement are included in Attachments B-1 and B-2 for Byron and Braidwood, resnectively. Improved Technical Specifications (ITS) are unaffected by this supplement since the value for RCS volume is not retained in ITS.
B. DESCRIPTION OF THE CURRENT REQUIREMENT The description of the current TS requirements remains unchanged from the .~anuary 30, 1997 submittal. Only the section pertaining to this supplement is provided here for reference.
TS 5.4.2 indicates 12,257 cubic feet for the total water and steam volume of the Reactor Coolant System at a nominal Tavg of 588.4 0F for each unit. This information is provided as part of the " Design Features" section of the Byron and Braidwood Technical Specifications and does not represent a limiting condition for operation.
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N C.' BASES FOR THE CURRENT REQUIREMENT The bases for the current TS requirements remains unchanged from the January 30,1997 submittal. Only the section pertaining to this supplement is provided here for reference.
TS 5.4.2 is a statement of the volume of the reactor coolant system with the plant in its original configuretion, which includes the Westinghouse Model D4 or D5 steam generators.
D. NEED FOR REVISION OF THE REQUIREMENT (SUPPLEMENTAL INFORMATION)
Each of the RSGs has a larger primary side volume than the OSGs. TS 5.4.2 provides information on the total RCS volume and requires a revision to reflect the volume increase associated with the Steam Generator Replacement Project. The original submittal dated January 30,1997 addressed only the increase associated with the RSGs.
Two issues have been identified which make the original submittal of the proposed revision to TS Section 5.4.2 in need of revision.
First, the B&W calculation for the RSG volume was reviewed as part of an NRC Region III Inspection.' As a result, it has been determined that the change in volume previously proposed for the RSGs is based on a cold volume and did not properly account for
- expansion factors at operating conditions (Tav3 at 588.4 F). As a result, the RSG 3
primary side volume reported in the original submittal (1251 ft ) must be increased by an additional 29 ft3, Second, Comed was notified by Westinghouse that the current TS value for Unit I and 2 total RCS volume (12,257 cubic feet) is not correct. The correction to the current TS value is an increase of 83 ft 3 to 12,340 ft 3. This increase applies to both units.
O As a result of the RCS volume increase with the RSGs, the mass and energy release during the blowdown phase of the large break Loss of Coolant Accident (LOCA)is increased for Unit 1. Additionally, the heat transfer rate of the RSGs is greater than the OSGs, and the RSGs will operate at a slightly higher secondary side pressure than that for the OSGs. Consequently, the steam enthalpy exiting the bre_al during the reflood period, for the RSG, will be greater than that for the OSG. This results in an increase in the containment peak pressure, Pa. The January 30,1997 submittal identified an increase in Pa from the current value of 44.4 psig to a value of 47.8 psig. This increase was calculated in the Containment LOCA Analysis performed by Framatome Technologies, Inc. (FTI) in support of the steam generator replacement project.
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S Margin is available in the Pa determination for the RSGs and the OSGs to offset the small volume increases addressed by this supplement. This margin will be explained in Section F of this attachment.
E. DESCRIPTION OF TIIE REVISED REQUIREMENT (SUPPLEMENTAL INFORMATION)
All descriptions of the revised requirements presented in the January 30,1997 submittal remain unchanged except for TS 5.4.2. The levisions to TS 5.4.2 are as follows:
Technical Specification Design Features Section 5.4.2 will be revised to incorporate the corrected total RCS volume and the corrected additional RCS volume associated with the RSGs.
For both Byron and Braidwood, the proposed changes to TS Section 5.4.2 are:
Revise the current RCS total volume from "12,257 cubic feet" to "12,340 cubic feet."
- Revise the additional RSG volume to "1280 cubic feet at a nominal Tavg of 588.4 F."
F. BASES FOR THE REVISED REQUIREMENT (SUPPLEMENTAL INFORMATION)
The January 30,1997 submittal provided the bases for the proposed change in Pa . The bases centered around the impact of the increased RCS volume associated with the RSGs.
This supplement further increases the RCS volume with the RSGs. Additionally, this supplement increases the total RCS volume for both Byron and Braidwood units to account for a calculational error in the determination of the TS value for the original RCS
. volume. The bases information provided in this section explains the proposed change in the RCS volumes and why the values of P a (current value and proposed Unit i value with RSGs) remains unchanged.
A11/itional Unit I and 2 RCS Volyme The TS states that the total volume of steam and water in the RCS is 12,257 ft3 at nominal operating conditions. Westingho"se notified Comed that there is an error in this number and that the correct value i,hould be 12,340 3ft . This applies to all four units at Byron and Braidwood. Westinghouse reviewed the original calculation of Pa for impacts of the higher volume. As a result of conservatisms, the original containment analysis calculation used an RCS volume of 12.619 ft3. The original containment analysis bounds the increase in RCS volume identified by Westinghouse and the current value of 44.4 psig for Pais unaffected.
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l Additional RSG Volume Ti e January 30,1997 submittal reported a chinge in RCS volume v.1251 ft 3 to account for the larger primary side volume of the RSGs. inis change in volume along with thermal hydraulic differences was used to calculate a change in Pa due to the RSGs.
However, the 1251 ft3 value was calculated as a cold volume, not at operating conditions.
This cold volume was used to calculate the changes in mass and energy release due to the RSGs and the result was added to the previous Westinghouse mass and energy release for the total RCS volume. A detailed discussion of this approach is presented in the May 23, 1997 Comed response to an NRC Request for Additional Information concerning the January 30,1997 submittal. The RCS volume basis in the earlier submittal for the determination of Pa was 13,870 ft3 (12,619 ft3 + 1251 ft3),
The additional 29 ft 3 increase in RCS volume associated with the RSGs is due to expansion factors. These expansion factors include: 1) thermal growth of the Inconel 690 tube material,2) pressure boundary dilation due to the primarf to secondary differential pressure, and 3) increase in ID of the steam generator tubes in the tubesheer stea due to the hydraulic expansion during the manufacturing process. The correcsd value for the increase in RCS volume due to the RSGs at operating conditions is 1280 ft3.
As previous!isuted, the corrected value for the existing RCS volume (at normal operating conditions)is 12 340 ft 3. The total RCS volume (at normal operating conditions) for the RSGs, then,is 13,620 ft3. The approv:d Westinghouse methodology adds an uncertainty of 1.4% for conservatism, resulting in a corrected value of 13,811 ft3 for calculatic tal purposes. Since this value is less than F.e 13,870 ft3 used to determine Pa in the January 30,1997 submittal, the 47.8 psig value is bounding and does not need to be changed as a result of the corrected RSG volume.
The bases discussions provided in the original January 30,1997 submittal remain unchanged except for the RCS volume section, TS 5.4.2. The revised basis is provided below.
The re.ised TS Design Features, TS 5.4.2 accounts for 1) the Unit 1 RSGs addition of a total of 1,280 cubic feet of vater volume to the RCS, and 2) a correction to the current RCS volume value to 12,340 cubic feet at nominal operating conditions. The effect of the increase in total RCS volume due to the RSGs was evaluated for all UFSAR, Chapter 15 accidents. The only impact on the Technical Specif, cations resulted from the increased mass and energy release following a LBLOCA event. The increased RCS volume was a cor.tributoi to the increase in the maximum calculated primary containment pressure, Pa , value. Therefore, the basis for acceptabiiity of the revised RCS volume is addressed by the basis for the Pa increase.
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G. IMPACT OF THE PROPOSED CHANGE (SUPPLEMENTAL INFORMATION) 1 This supplement to the January 30,1997 submittal addresses the changes necessary to l account for increased RCS volumes in both Units 1 and 2 at Byron and Braidwood. As l 2xplained in Section F of this attachment, the increases in RCS volume do not alter either 4
the proposed change in Pa for ute RSGs nor the current OSG value of Pa. Therefore, the impact of the proposed change as discussed in the original submittal remains unchanged.
Any impacts on Unit 2 from an increase in RCS volume, other than Pa, are bounded by the evaluations presented for Unit I with the RSGs since the total increase in volume with the RSGs is significantly greater than the proposed change in the Unit 2 RCS volume.
The potential impact of increase RCS volumes on post-LOCA conditions has also been evaluated for both units The impact on maximum 'looding levels, post-accident sump pH, and post-accident hydrogen generation has be erformed. These parameters remain within allowable values.
H. SCHEDULE REQUIREMENTS The Byron Unit 1 Steam Generator Replacement Outage (SGRO)is scheduled during the eighth refuel outage (BiR08). The Braidwood Unit 1 SGRO is scheduled during the
, seventh refuel outage (A1R07). Approval of this change (as supplemented by this attachment) is requested as soon as possible to support the current outage schedule for the l lead steam generator replacement station which is Byron Unit 1. I i
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l ATTACHMENT B-1 l MARKED UP PAGES COR .
?- PROPOSED CHANGES TO AP?ENDIX A TECHNICAL SPECIFICATIOdS OF FACILITY OPERATING LICEhJES l- NPF-37, NPF-66 BYRON STATION UNITS 1 & 2 REVISED SUPPLEMENT PAGE:
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