ML20071L650: Difference between revisions

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| number = ML20071L650
| number = ML20071L650
| issue date = 04/26/1983
| issue date = 04/26/1983
| title = Responds to NRC 830401 Ltr Re Violations Noted in IE Insp Rept 50-400/83-06.Corrective Actions:Addl Supports Added to Two Svc Water Piping Spool Pieces to Comply W/Procedural requirements,WP-102,App a
| title = Responds to NRC Re Violations Noted in IE Insp Rept 50-400/83-06.Corrective Actions:Addl Supports Added to Two Svc Water Piping Spool Pieces to Comply W/Procedural requirements,WP-102,App a
| author name = Parsons R
| author name = Parsons R
| author affiliation = CAROLINA POWER & LIGHT CO.
| author affiliation = CAROLINA POWER & LIGHT CO.
Line 12: Line 12:
| case reference number = CON-NRC-62
| case reference number = CON-NRC-62
| document report number = NUDOCS 8305270615
| document report number = NUDOCS 8305270615
| title reference date = 04-01-1983
| package number = ML20071L627
| package number = ML20071L627
| document type = CORRESPONDENCE-LETTERS, INCOMING CORRESPONDENCE, UTILITY TO NRC
| document type = CORRESPONDENCE-LETTERS, INCOMING CORRESPONDENCE, UTILITY TO NRC

Latest revision as of 02:50, 31 May 2023

Responds to NRC Re Violations Noted in IE Insp Rept 50-400/83-06.Corrective Actions:Addl Supports Added to Two Svc Water Piping Spool Pieces to Comply W/Procedural requirements,WP-102,App a
ML20071L650
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 04/26/1983
From: Parsons R
CAROLINA POWER & LIGHT CO.
To: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20071L627 List:
References
CON-NRC-62 NUDOCS 8305270615
Download: ML20071L650 (2)


Text

__

eCp&L Carolina Powerg Ligt Company

,-shv, , . . . . . . ~ - _

N 'O P. Q.\Yox 101, New Hill, N. C. 27562 .

April 26, 1983 Mr. James P. O'Reilly NRC-62 United States Nuclear Regulatory Commission Region II 101 Marietta Street, Northwest (Suite 3100)

Atlanta, Georgia 30303

Dear Mr. O'Reilly:

In reference to your letter of April 1, 1983, referring to RII: GFM 50-400/83-06, the attached is Carolina Power and Light Company's reply to the violation identi-fied in Appendix A.

It is considered that the corrective action taken is satisfactory for resolution of the item.

Thank you for your consideration in this matter.

Yours very truly,

' W R. M. Parsons A a w A 0i ?" d Project General Manager Shearon Harris Nuclear Power Plant RMP/sh Attachment cc: Mr. P. Kadambi (NRC)

Mr. R. Prevatte (NRC-SHNPP)

Mr. G. F. Maxwell (NRC-SHNPP) l i

O h PDR l

l

Attachment to CP&L Letter of Response to NRC Report RII: .GFM 50-400/83-06 Reported Violation:

10 CFR 50, Appendix B, Criterion V as implemented by PSAR Section 1.8.5.5 and.CP&L's Corporate QA Program Section 6.2.5 requires that activities?

affecting quality be accomplished in accordance with procedures.

Contrary to the above, on January 26, 1983, two service water piping spool pieces were found to be unsupported at the 30 foot. intervals which are required by construction procedure WP-102, Appendix A.. One of the spool pieces, partially-filled with water, was found unsupported for a distance of 31 1/2 feet, and the other piece was found. unsupported for a distance of 74 feet. Site records indicate that CP&L inspection personnel have identified at least five similar procedural violations in the last year involving' failure to adequately support' piping spool' pieces.

This is a Severity Level V Violation (Supplement L II.E.).

Denial or Admission and Reason for the Violation:

The violation is correct as stated. Responsible piping craft-personnel did not understand the procedural requirements or did not adequately monitor other craft activity in the area to control unauthorized removal of supports.

Corrective Steps Taken and Results Achieved:

Additional supports were added to comply with' procedural requirements of WP-102, Appendix A. Lines were evaluated for overstress and stress levels imposed were within acceptable levels. See NCR-M-223 and NCR-M-224 for calculations.

Corrective Steps Taken to Avoid Further Noncompliance:

The Daniel Mechanical' Manager, CP&L Resident Engineer, and CP&L-Lead Piping.

Engineer investigated the incident and the responsible supervisor was instructed in WP-102 requirements. Additionally, . training was held in February,1983 under the Quality Improvement Program for all piping craft supervisors. As evidence of the training effectiveness, CI performed two surveillance tours per week, an'd' for the five-week period ending April 15,~1983, no violations have been detected.

Date When Full Compliance Will Be Achieved:

Full compliance was achieved on March 1, 1983.

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