IR 05000266/2007002: Difference between revisions
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{{#Wiki_filter: | {{#Wiki_filter:ril 12, 2007 | ||
==SUBJECT:== | |||
POINT BEACH NUCLEAR PLANT, UNITS 1 AND 2, NRC INTEGRATED INSPECTION REPORT 05000266/2007002 AND 05000301/2007002 | |||
==Dear Mr. Koehl:== | ==Dear Mr. Koehl:== | ||
On March 31, 2007, the U.S. Nuclear Regulatory Commission (NRC) completed an | On March 31, 2007, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated inspection at your Point Beach Nuclear Plant, Units 1 and 2. The enclosed inspection report documents the inspection results, which were discussed on April 3, 2007, with you and members of your staff. | ||
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations, and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed your personnel. | |||
Based on the results of this inspection, two findings of very low safety significance associated with violations of NRC requirements were identified. However, because of the very low safety significance and because they are entered into your corrective action program, the NRC is treating these findings as non-cited violations (NCVs) consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest any NCV in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with copies to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector at the Point Beach Nuclear Plant. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records System (PARS) | |||
component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). | component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). | ||
Sincerely, | Sincerely, | ||
/RA/Patrick L. Louden, | /RA/ | ||
Patrick L. Louden, Chief Branch 5 Division of Reactor Projects Docket Nos. 50-266; 50-301 License Nos. DPR-24; DPR-27 Enclosure: Inspection Report 05000266/2007002; 05000301/2007002 w/Attachment: Supplemental Information cc w/encl: F. Kuester, President and Chief Executive Officer, We Generation D. Cooper, Senior Vice President and Chief Nuclear Officer J. McCarthy, Site Director of Operations D. Weaver, Nuclear Asset Manager Plant Manager Regulatory Affairs Manager Training Manager Site Assessment Manager Site Engineering Director Emergency Planning Manager J. Rogoff, Vice President, Counsel & Secretary K. Duveneck, Town Chairman Town of Two Creeks Chairperson Public Service Commission of Wisconsin J. Kitsembel, Electric Division Public Service Commission of Wisconsin State Liaison Officer | |||
=SUMMARY OF FINDINGS= | =SUMMARY OF FINDINGS= | ||
IR 05000266/2007002 and 05000301/2007002; 01/01/2007 - 03/31/2007; Point Beach | IR 05000266/2007002 and 05000301/2007002; 01/01/2007 - 03/31/2007; Point Beach Nuclear | ||
Plant, Units 1 and 2; Adverse Weather Protection; and Event Followup. | |||
This report covers a 3-month period of inspections by resident inspectors and regional specialists. Two Green findings with associated non-cited violations were identified. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000. | |||
A. Inspector-Identified and Self-Revealed Findings | |||
===Cornerstone: Initiating Events=== | ===Cornerstone: Initiating Events=== | ||
: '''Green.''' | : '''Green.''' | ||
The inspectors identified a finding and associated non-cited violation(NCV) of 10 CFR Part 50, Appendix B, Criterion XVI, | The inspectors identified a finding and associated non-cited violation (NCV) of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, having very low safety significance (Green) for the failure to take prompt corrective actions to address a potential cold weather issue initially identified in October 2006 and again in January 2007. The failure to take prompt corrective actions led to the formation of ice on offsite power and plant equipment cable trays and cabling. The sheets of ice were also in close proximity to the Unit 2 Refueling Water Storage Tank level indicators and outlet piping. The licensee initiated condition reports and took immediate corrective actions and had planned additional corrective actions based on a causal evaluation. | ||
The finding is greater than minor because if left uncorrected the finding would become a more significant safety concern in that the formation of ice in the facade building in this case could have affected safety-related equipment. In addition, the finding is associated with the external factors attribute of the Initiating Events cornerstone and affected the cornerstone objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Because the significant ice buildup in the Unit 2 facade was an external factor and transient initiator contributor, and did not contribute to both the likelihood of both a reactor trip and that mitigation equipment or functions would not be available, the finding is considered to be of very low safety significance (Green). This finding has a cross-cutting aspect in the area of problem identification and resolution because the licensee did not take appropriate corrective actions in a timely manner, commensurate with their safety significance and complexity. (Section 1R01) | |||
===Cornerstone: Barrier Integrity=== | ===Cornerstone: Barrier Integrity=== | ||
* Green: A non-cited violation (NCV) of 10 CFR 50, Appendix B, Criterion III, | |||
Design Control, having very low safety significance was self-revealed for the failure to maintain sufficient design margin for the expected running currents of the control room emergency filtration system fans to their thermal overload trip settings. This occurred due to design errors in a modification that replaced the fans in October 2006. Control Room Emergency Filtration System (CREFS) | |||
Fan W-1-B tripped on a breaker thermal overload during surveillance testing in February 2007 with low outside ambient air temperature (approximately negative 11EFahrenheit). Licensee analyses also demonstrated that a trip of fan W-14A could have occurred for the combination of low ambient temperature and degraded grid voltage. The licensee took immediate corrective actions to replace the breaker thermal overloads with thermal overloads of a higher setting as a result of troubleshooting and evaluations performed following the trip of the W-14B fan. The issue was entered into the licensees corrective action program and a root cause evaluation was subsequently performed. | |||
The finding is greater than minor because it is associated with the attribute of maintaining radiological barrier functionality of the control room and affected the Barrier Integrity cornerstone objective to provide reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events. Loss of CREFS fans during a release could result in increased dose to the operators in the control room potentially affecting control room habitability. Although the finding involved a potential failure of the CREFS to provide its filtration function, the simultaneous occurrence of low outside air temperature, degraded grid voltage, and a radiological release is of very low probability. The finding for the failure to provide the correct thermal overload trip setting is a design deficiency that has a cross-cutting aspect in the area of human performance in that resources were not effective in maintaining long-term plant safety by maintenance of design margins. (Section 4OA3) | |||
=REPORT DETAILS= | |||
===Summary of Plant Status=== | |||
Unit 1 was at 100 percent power throughout the inspection period with the exception of brief downpowers during routine auxiliary feedwater and secondary system valve testing and until March 31, 2007, when the unit was shutdown to commence U1R30 refueling outage. | |||
Unit 2 was at 100 percent power throughout the inspection period with the exception of brief downpowers during routine auxiliary feedwater and secondary system valve testing. | |||
= | ==REACTOR SAFETY== | ||
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity {{a|1R01}} | |||
==1R01 Adverse Weather Protection== | |||
{{IP sample|IP=IP 71111.01}} | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors walked down accessible portions of risk-significant equipment | The inspectors walked down accessible portions of risk-significant equipment and systems susceptible to cold weather freezing during the onset of cold weather. The inspectors walked down all accessible portions of the Units 1 and 2 facade buildings, which enclosed the reactor containments and certain plant equipment inside the protected area. The inspectors reviewed the corrective actions and work orders (WOs)written to correct identified problems. The inspectors also walked down areas which had a history of freeze problems. This observation constituted one inspection procedure system sample. | ||
====b. Findings==== | ====b. Findings==== | ||
=====Introduction:===== | =====Introduction:===== | ||
The inspectors identified a finding and associated non-cited violation(NCV) of 10 CFR Part 50, Appendix B, Criterion XVI, | The inspectors identified a finding and associated non-cited violation (NCV) of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, having very low safety significance (Green) for the failure to take prompt corrective actions to address a potential cold weather issue initially identified in October 2006 and again in January 2007. The failure to take prompt corrective actions led to the formation of ice on offsite power and plant equipment cable trays and cabling. The sheets of ice were also in close proximity to the Unit 2 Refueling Water Storage Tank (RWST) level indicators and outlet piping. | ||
=====Description:===== | =====Description:===== | ||
On February 6, 2007, plant staff identified that in the Unit 2 | On February 6, 2007, plant staff identified that in the Unit 2 containment facade a wall of ice had formed on cable trays and portions of cabling within the trays. | ||
The containment facade is an unheated structure surrounding the containment building which contains some plant electrical equipment and other various safety-related equipment, such as the RWST. The cable trays contained the offsite power lines from a Unit 2 transformer to the associated busses, in addition to various equipment cabling. | The containment facade is an unheated structure surrounding the containment building which contains some plant electrical equipment and other various safety-related equipment, such as the RWST. The cable trays contained the offsite power lines from a Unit 2 transformer to the associated busses, in addition to various equipment cabling. | ||
The ice had formed on either side of the cable tray, and had a maximum dimension on one side of the cable tray of approximately 15 feet high by 6 feet wide and a thickness of greater than 1 inch. Operations staff immediately requested walkdowns from system | The ice had formed on either side of the cable tray, and had a maximum dimension on one side of the cable tray of approximately 15 feet high by 6 feet wide and a thickness of greater than 1 inch. Operations staff immediately requested walkdowns from system and structural engineers to determine the structural acceptability of the trays current state which were judged satisfactory. The ice wall and cable trays were approximately 5 feet away from the RWST and near the outlet piping for the RWST, the inlet for the RWST minimum flow recirculation piping, and the level transmitters for the RWST. | ||
Operations directed maintenance craft to create a tent with a temporary heat source to melt the ice and redirect the source of water.On February 7, 2007, the inspectors walked down the Unit 2 facade and | Operations directed maintenance craft to create a tent with a temporary heat source to melt the ice and redirect the source of water. | ||
On February 7, 2007, the inspectors walked down the Unit 2 facade and questioned whether: the melting icicles presented a threat to the equipment below; certain junction boxes covered in ice would be affected by the water as the ice was melted; and certain portions of the facade freeze system were in jeopardy of not functioning due to the melting ice. Operations and engineering determined that no adverse conditions existed and additional operator walkdowns were performed of the facade freeze system (which prevents safety-related lines from freezing during cold weather) and area. The licensee also determined the source of the water was a leaking steam relief valve in the radioactive waste system. The relief valve was located on the 46-foot elevation of the facade and the steam normally relieved into the Primary Auxiliary Building Relief Stack located adjacent to the RWST. The licensee continued with actions to melt the ice on the trays, monitor the area and redirect the water. Finally, the inspectors noted that Condition Report AR0107430, written in January 2007, identified the leaking relief valve and stated that the issue would be a problem when colder weather arrived. The inspectors also identified to the licensee that the condition report appeared to have been inadvertently closed 1 week prior with no actions taken. Finally, the inspectors learned from discussions with plant staff that this area had experienced ice formation in prior years, although no corrective action documentation was found. | |||
On February 8, 2007, the inspectors again walked down the facade and concluded that the relief vent stack, approximately 20 inches in diameter, was most likely filled with a combination of ice and water and noted that the licensee still had not taken any action to address the source of the leak. The inspectors also questioned whether the licensee had considered the potential adverse affects of the relief stack, likely filled with ice and water to a height of approximately 40 feet, near the Unit 2 RWST. The licensee performed additional evaluations to provide reasonable assurance that the vent line would remain intact during a seismic event and initiated actions to thaw the frozen relief stack drain. The thawing of the relief vent stack drain resulted in the sudden removal of a large volume of water from the relief vent stack, along with the melting of ice within the relief stack. In addition, the licensee took immediate corrective actions to replace the leaking relief valve to isolate the source of water. | |||
The licensee subsequently performed an apparent cause evaluation and identified that a second Condition Report, AR01054609, was written in October 2006 identifying the leaking relief valve and the fact this would become a cold weather issue. The condition report was closed to a work request at that time, and neither the condition report, nor the work request were flagged in the licensees work order and corrective action systems as a cold weather issue. The January 2007 condition report was also not flagged as a cold weather issue and was inadvertently closed due to an inadequate communication. Therefore, multiple barriers, including the corrective action program screening team and work request screening team, failed to identify and track this cold weather issue. The licensee also determined the relief valve vent stack drain froze due to abandonment of the heat trace circuit during the facade freeze heat trace upgrade project in 1999. The licensee subsequently determined as a result of the extent of condition that an additional 40 circuits were abandoned in 1999 with no documentation justifying that action. Finally, as a result of increased attention in this area, the licensee identified an additional 5 facade cold weather issues, which were addressed. | |||
=====Analysis:===== | =====Analysis:===== | ||
The inspectors determined that the | The inspectors determined that the licensees failure to implement prompt corrective actions to correct equipment deficiencies prior to the onset of cold weather, which could have significantly impacted safety-related equipment, was a performance deficiency requiring a significance evaluation. Using IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue Screening, dated November 2, 2006, the inspectors concluded that the finding is greater than minor because if left uncorrected the finding would become a more significant safety concern in that the formation of ice in the facade building in this case could have affected safety-related equipment. In addition, the finding is associated with the external factors attribute of the Initiating Events cornerstone and affected the cornerstone objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. | ||
The inspectors evaluated the finding using IMC 0609, Significance Determination Process, Appendix A, Determining the Significance of Reactor Inspection Findings for At-Power Situations, dated November 22, 2005. The transient initiator contributor was the external factor of significant ice buildup in the Unit 2 facade, and did not contribute to both the likelihood of both a reactor trip and that mitigation equipment or functions would not be available. Consequently, the finding is considered to be of very low safety significance (Green). | |||
The inspectors also determined that a primary cause of this finding is related to the cross-cutting area of problem identification and resolution. Specifically, under the component of corrective action program, the licensee failed to ensure the aspect of taking appropriate corrective actions to address safety issues in a timely manner, which directly contributed to this performance deficiency. | |||
=====Enforcement:===== | =====Enforcement:===== | ||
10 CFR Part 50, Appendix B, Criterion XVI, | 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, states, in part, that measures shall be established to assure that conditions adverse to quality, such as deficiencies, deviations, and nonconformances, are promptly identified and corrected. Contrary to this, the licensee was made aware of a condition adverse to quality associated with the leaking relief valve on two occasions in October 2006 and January 2007 and did not take prompt corrective actions to correct the condition prior to the onset of cold weather and potential impacts on safety-related systems. The failure to implement prompt corrective actions for these conditions adverse to quality is a violation of 10 CFR Part 50, Appendix B, Criterion XVI. Because of the very low safety significance of this finding and because the issue was entered into the licensees corrective action program (AR01075828), it is being treated as an NCV, consistent with Section VI.A.1 of the Enforcement Policy (NCV 05000301/2007002-01). | ||
As stated previously, the licensee took corrective actions to correct the condition upon discovery and performed an apparent cause evaluation. Additional actions taken to address the apparent cause that the corrective action and work request screening teams failed to properly classify work request and condition reports as cold weather issues and subsequently assign timely corrective actions included: actions to both teams to review the event and procedure expectations regarding assigning the proper attributes for any condition to condition reports and work requests; an informational bulletin was sent to plant personnel to ensure the appropriate attributes are contained on work requests; operations staff reviewed the event and reinforced expectations regarding log entries, turnover information, and documentation of condition reports; the 40 abandoned circuits were evaluated to determine which require re-energization; re-energization of the relief valve vent stack facade freeze protection circuit; determination whether the RWST vent lines require freeze protection; and determination if any configuration changes were required for sample and drain locations in the facades. | |||
{{a|1R04}} | {{a|1R04}} | ||
==1R04 Equipment Alignment | ==1R04 Equipment Alignment== | ||
{{IP sample|IP=IP 71111.04}} | |||
===.1 Partial System Walkdowns=== | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors performed partial walkdowns of accessible portions of risk- | The inspectors performed partial walkdowns of accessible portions of risk-significant systems to determine the operability of the systems. The inspectors utilized system valve lineup and electrical breaker checklists, tank level books, plant drawings, and selected operating procedures to determine if the systems were correctly aligned to perform the intended design functions. The inspectors also examined the material condition of the components and observed operating equipment parameters to determine whether deficiencies existed. The inspectors reviewed completed work orders (WOs) and calibration records associated with the systems for issues that could affect component or train functions. The inspectors used the information in the appropriate sections of the Final Safety Analysis Report (FSAR) to determine the functional requirements of the system. Partial system walkdowns of the following systems constituted three inspection procedure samples: | ||
*Unit 1 Component Cooling Water (CCW). | * Service Water Trains A, B, and C; | ||
* Service Water Trains D, E, and F; and | |||
* Unit 1 Component Cooling Water (CCW). | |||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified.. | No findings of significance were identified. | ||
===.2 Complete System Walkdowns=== | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors performed a complete system alignment inspection of the | The inspectors performed a complete system alignment inspection of the Auxiliary Feedwater (AFW) system for Units 1 and 2. This safety-related system was selected based on the risk-significance of the system in the licensees probabilistic risk assessment. The walkdown of the AFW constituted one semiannual inspection procedure sample. | ||
*Review of plant procedures (including selected abnormal and | |||
The inspection consisted of the following activities: | |||
* Review of plant procedures (including selected abnormal and emergency procedures), drawings, and the FSAR to identify proper system alignment; | |||
* Review of outstanding or completed temporary and permanent modifications to the system; | |||
* Review of open corrective action program documents (CAP ARs) and WOs that could impact operability of the system; and | |||
* Walkdown of mechanical and electrical components in the system to assess alignment, component accessibility, availability, and current condition. | |||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. | No findings of significance were identified. {{a|1R05}} | ||
{{a|1R05}} | ==1R05 Fire Protection== | ||
==1R05 Fire Protection | {{IP sample|IP=IP 71111.05}} | ||
===.1 Walkdown of Selected Fire Zones=== | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors conducted fire protection walkdowns which focused on the | The inspectors conducted fire protection walkdowns which focused on the following attributes: the availability, accessibility, and condition of fire fighting equipment; the control of transient combustibles and ignition sources; and the condition and status of installed fire barriers. The inspectors selected fire areas for inspection based on the areas overall fire risk contribution, as documented in the Individual Plant Examination of External Events, or the potential of a fire to impact equipment that could initiate a plant transient. | ||
*Fire Zone 153/Fire Area A04; Charging Pump 1P2B; | |||
*Fire Zone 771/Fire Area A61; Fuel Oil Pump Room. | In addition, the inspectors assessed these additional fire protection attributes during walkdowns: fire hoses and extinguishers were in the designated locations and available for immediate use; unobstructed fire detectors and sprinklers; transient material loading within the analyzed limits; and fire doors, dampers, and penetration seals in satisfactory condition. The inspectors also determined if minor issues identified during the inspection were entered into the licensees corrective action program. The walkdown of the following selected fire zones constituted eight inspection procedure samples: | ||
* Fire Zone FZ596/Fire Area A01-H; Unit 2 Containment Facade; | |||
* Fire Zone 156/Fire Area A06; MCC 1B32 and Fire Zone 154/Fire Area A05; Charging Pump 1P2A; | |||
* Fire Zone 166/Fire Area A15; MCC 2B32 and Fire Zone 155/Fire Area A05; Charging Pump 2P2A; | |||
* Fire Zone 152/Fire Area A03; Charging Pump 1P2C; | |||
* Fire Zone 153/Fire Area A04; Charging Pump 1P2B; | |||
* Fire Zone 163/Fire Area A12; Charging Pump 2P2C; | |||
* Fire Zone 164/Fire Area A13; Charging Pump 1P2B; and | |||
* Fire Zone 771/Fire Area A61; Fuel Oil Pump Room. | |||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified..2(Open) Unresolved Item (URI 05000266/2004010-01; 05000301/2004010-01) -Operational Implementation of Alternate Shutdown | No findings of significance were identified. | ||
===.2 (Open) Unresolved Item (URI 05000266/2004010-01; 05000301/2004010-01) -=== | |||
Operational Implementation of Alternate Shutdown Capability The Point Beach Nuclear Plant (PBNP) Fire Protection Program (FPP) described the means by which safe shutdown could be achieved to meet the requirements of 10 CFR Part 50, Appendix R, Sections III.G.3 and III.L. The PBNP safe shutdown analysis identified the minimum number of components and plant systems necessary for achieving Appendix R safe shutdown performance goals. The FPP accomplished safe shutdown by isolating power to most plant equipment and then used an emergency diesel generator or the station blackout turbine generator to power equipment necessary for plant shutdown. Numerous manual actions were required with four operations staff working together to shutdown both Unit 1 and Unit 2. | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors performed a review of licensee actions | The inspectors performed a review of licensee actions regarding URI 05000266/2004010-01; 05000301/2004010-01. This URI was associated with a lack of time for critical manual actions in Abnormal Operating Procedure (AOP) AOP-10A, Safe Shutdown - Local Control, Revision 39, and AOP 10C, Safe Shutdown Following a Fire at PAB [Primary Auxiliary Building] 26 Foot Central, Revision 0. The fire protection procedures were common to both units and were to be implemented as fire area specific (i.e., alternate shutdown (ASD)) | ||
procedures for the Control Room, Cable Spreading Room, and the 26-foot elevation of the PAB. The inspectors reviewed the | procedures for the Control Room, Cable Spreading Room, and the 26-foot elevation of the PAB. The inspectors reviewed the licensees evaluation for these procedures. | ||
In addition, the inspectors reviewed the licensee actions regarding Fire Operating Procedure (FOP) 1.2, | In addition, the inspectors reviewed the licensee actions regarding Fire Operating Procedure (FOP) 1.2, Potential Fire Affected Safe Shutdown Equipment, Revision 15, which had not previously identified time critical manual actions for plant fire scenarios. | ||
The inspectors reviewed the | The inspectors reviewed the licensees evaluation for time critical manual actions and changes to this procedure. | ||
=====Description:===== | =====Description:===== | ||
The URI issue for procedures AOP-10 and FOP 1.2 regarded | The URI issue for procedures AOP-10 and FOP 1.2 regarded the potential for not having adequate water inventory available for reactor makeup during the 72 hours required to reach cold shutdown because of Reactor Coolant Pump (RCP) leakage and the potential drain down of the RWST (i.e., through a spuriously operated valve to the containment sump) from an Appendix R Fire. As a result, the inspectors were concerned that the licensee had the potential for a non-conservative Appendix R manual action response time in their procedures for ensuring that the RWST was isolated from draining to the containment. | ||
The licensee initiated a CAP to formalize a previously unapproved evaluation and prepare a new calculation for the AOP-10 manual actions. The licensee entered this issue into their corrective action program as CAP060624, Potentially Non-Conservative Appendix R Response Times, dated November 18, 2004. The licensee completed a review and performed a new calculation to resolve the AOP issue. The licensee performed Calculation WE00010-05, Revision 0, which indicated that adequate time existed to close RWST valves to the containment and maintain an adequate inventory of water in the RWST. The inspectors reviewed this calculation and verified that adequate time existed to isolate the valves to containment and ensure a safe shutdown of the plant. This portion of the URI is considered closed. | |||
The inspectors had identified a similar issue where the licensee did not identify the time critical manual actions in FOP 1.2, Potential Fire Affected Safe Shutdown Equipment, Revision 6. However, unlike the AOP-10 procedures, with step by step operator actions to shut down the plant, these procedures were symptom-based, making it difficult to identify a spurious actuation and take a manual action. For example, fires in certain fire areas required time critical manual actions, to ensure that the RWST is isolated to prevent drain down of water to the containment sump. As a result of the inspectors concern, the licensee issued CAP 060641, FOP 1.2 Enhancement Recommendation, November 19, 2004, to review this issue. During the resolution of this issue, the licensee initiated compensatory actions, such as, assigning hourly fire rounds for all areas where a fire could potential cause a spurious actuation and a subsequent drain down of the RWST. The licensees corrective actions included identifying time critical manual actions in this procedure and then prioritizing those manual actions that needed to be performed early during fire scenarios. | |||
However, the inspectors noted that the licensee took credit in its evaluation for a third valve (Valve 1/2SI 851 A/B) with an unknown leakage rate in the RWST piping. In addition, the licensee had not identified the location of the control circuitry, torque, and limit switch wiring for this valve nor evaluated fire scenarios for this wiring. Additionally, the licensee used only a single spurious actuation per fire to resolve this issue. | |||
Reliance upon a single spurious actuation was inconsistent with the licensees Safe Shutdown Analysis Report (SSAR) and Fire Protection Evaluation Report (FPER). The use of a single spurious actuation per fire area during fire scenarios is an issue that continues to be evaluated by the NRC. As a result, this portion of the URI remains open pending regulatory resolution of the fire protection circuits generic issue. | |||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified.. | No findings of significance were identified. {{a|1R11}} | ||
==1R11 Licensed Operator Requalification== | |||
{{IP sample|IP=IP 71111.11}} | |||
===.1 Resident Inspector Quarterly Observation of Licensed Operator Requalification=== | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
On February 15, 2007, the inspectors observed the operating crew performance during a simulator as-found requalification examination. Observation of the requalification quarterly evaluation constituted one inspection procedure sample. | |||
The | The inspectors assessed crew performance in the areas of: | ||
* Clarity and formality of communications; | |||
* Understanding of the interactions and function of the operating crew during an emergency; | |||
* Prioritization, interpretation, and verification of actions required for emergency procedure use and interpretation; | |||
* Oversight and direction from supervisors; and | |||
* Group dynamics. | |||
Crew performance in these areas was also compared to licensee management expectations and guidelines, as presented in nuclear plant procedure NP 2.1.1, Conduct of Operations. The inspectors also verified that the licensee and crew assessed and critiqued crew performance accordingly. | |||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. | No findings of significance were identified. | ||
===.2 Operating Test Results=== | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors reviewed the overall pass/fail results of the comprehensive annual job performance measure operating tests, the annual simulator operating tests, and the biennial written examinations (required to be given per 10 CFR 55.59(a)(2)). The operating tests were administered by the licensee from August through October 2006. | |||
The written examinations were conducted during December 2006. The overall results were compared with the significance determination process in accordance with NRC Manual Chapter 0609, Appendix I, Operator Requalification Human Performance Significance Determination Process (SDP). | |||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. | No findings of significance were identified. {{a|1R12}} | ||
{{a| | ==1R12 Maintenance Effectiveness== | ||
== | {{IP sample|IP=IP 71111.12}} | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors reviewed | The inspectors performed maintenance effectiveness reviews of the systems listed below. The inspectors reviewed repetitive maintenance activities to assess maintenance effectiveness, including maintenance rule activities, work practices, and common cause issues. Inspection activities included, but were not limited to, the licensee's categorization of specific issues, including evaluation of performance criteria, appropriate work practices, identification of common cause errors, extent of condition, and trending of key parameters. Additionally, the inspectors reviewed implementation of the Maintenance Rule (10 CFR 50.65) requirements, including a review of scoping, goal-setting, performance monitoring, short-term and long-term corrective actions, functional failure determinations, and current equipment performance status. | ||
For each system reviewed, the inspectors reviewed significant WOs and CAPs to determine if failures were appropriately identified, classified, and corrected, and if unavailable time was correctly calculated. The reviews of maintenance effectiveness for the following components and systems constituted two inspection procedure samples: | |||
* 125-V DC Safety-Related Battery Chargers, D-07, D-08, D-09, D-107, D-108 and D-109; and | |||
* 125-V DC Safety-Related Batteries D-05, D-06, D-105, D-106, and D-305. | |||
* | |||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. | No findings of significance were identified. {{a|1R13}} | ||
{{a| | ==1R13 Maintenance Risk Assessment and Emergent Work Evaluation== | ||
== | {{IP sample|IP=IP 71111.13}} | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors reviewed | The inspectors reviewed risk assessments for planned and emergent maintenance activities during the specified work weeks. During these reviews, the inspectors compared the licensees risk management actions to those actions specified in the licensees procedures for the assessment and management of risk associated with maintenance activities. The inspectors assessed whether evaluation, planning, control, and performance of the work were done in a manner to reduce the risk and minimize the duration where practical, and whether contingency plans were in place where appropriate. | ||
The inspectors used the licensees daily configuration risk assessment records, observations of shift turnover meetings, and observations of daily plant status meetings to determine if the equipment configurations were properly listed. The inspectors also verified that protected equipment was identified and controlled as appropriate, and that significant aspects of plant risk were communicated to the necessary personnel. The reviews of maintenance risk assessment and emergent work evaluation constituted seven inspection procedure samples: | |||
* Planned and emergent maintenance during the week of January 21, 2007; | |||
* Planned and emergent maintenance during the week of February 4, 2007; | |||
* Planned and emergent maintenance during the week of February 12, 2007; | |||
* Planned and emergent maintenance during the week of February 18,2007; | |||
* Planned and emergent maintenance during the week of March 4, 2007; | |||
* Planned and emergent maintenance during the week of March 11, 2007; and | |||
* Planned and emergent maintenance during the week of March 26, 2007. | |||
====b. Findings==== | |||
No findings of significance were identified. {{a|1R15}} | |||
==1R15 Operability Evaluations== | |||
{{IP sample|IP=IP 71111.15}} | |||
samples:*AR1080577, RCS Flow Uncertainty Measurements;*OBD for AR1043614, Battery D-06 Decreasing Specific Gravity Trends; | ====a. Inspection Scope==== | ||
*AR1075828, Operability Assessment for Facade Freezing; and | The inspectors reviewed selected operability evaluations (OPRs) associated with issues entered into the licensees corrective action program. The inspectors reviewed design basis information, the FSAR, Technical Specification (TS) requirements, and licensee procedures to determine the technical adequacy of the operability evaluations. In addition, the inspectors determined if compensatory measures were implemented, as required. The inspectors assessed whether system operability was properly justified and that the system remained available, such that no unrecognized increase in risk occurred. The reviews of the following operability evaluations constituted four procedure samples: | ||
*AR1068922, Issues with CCW Containment Penetrations Unit 1 P-20 &Unit 2 P-19. | * AR1080577, RCS Flow Uncertainty Measurements; | ||
* OBD for AR1043614, Battery D-06 Decreasing Specific Gravity Trends; | |||
* AR1075828, Operability Assessment for Facade Freezing; and | |||
* AR1068922, Issues with CCW Containment Penetrations Unit 1 P-20 & | |||
Unit 2 P-19. | |||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. | No findings of significance were identified. {{a|1R19}} | ||
{{a|1R19}} | |||
==1R19 Post-Maintenance Testing== | ==1R19 Post-Maintenance Testing== | ||
{{IP sample|IP=IP 71111.19}} | {{IP sample|IP=IP 71111.19}} | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
During completion of the post-maintenance test inspection procedure samples, | During completion of the post-maintenance test inspection procedure samples, the inspectors observed in-plant activities and reviewed procedures and associated records to determine if: | ||
* Testing activities satisfied the test procedure acceptance criteria; | |||
*Measuring and test equipment calibration was current; | * Effects of the testing were adequately addressed prior to the testing; | ||
*Test equipment was within the required range and accuracy; | * Measuring and test equipment calibration was current; | ||
*Applicable prerequisites described in the test procedures were satisfied; | * Test equipment was within the required range and accuracy; | ||
*Affected systems or components were removed from service in | * Applicable prerequisites described in the test procedures were satisfied; | ||
*Test data and results were accurate, complete, and valid; | * Affected systems or components were removed from service in accordance with approved procedures; | ||
*Test equipment was removed after testing; | * Testing activities were performed in accordance with the test procedures and other applicable procedures; | ||
*Equipment was returned to a position or status required to support the | * Jumpers and lifted leads were controlled and restored where used; | ||
*Unit 1 Containment Spray Inservice Test of Pumps and Valves | * Test data and results were accurate, complete, and valid; | ||
*1P-10A Residual Heat Removal pump motor MCE/EMAX and return | * Test equipment was removed after testing; | ||
* Equipment was returned to a position or status required to support the operability of the system in accordance with approved procedures; and | |||
* All problems identified during the testing were appropriately entered into the corrective action program. | |||
The activities listed below were reviewed by the inspectors and constituted seven quarterly inspection procedure samples: | |||
* Emergency Diesel Generator G-03 Governor testing on January 9, 2007; | |||
* Emergency Diesel Generator G-03 Governor testing on January 11, 2007; | |||
* Unit 1 Containment Spray Inservice Test of Pumps and Valves on January 17,2007; | |||
* Unit 1 Manually Operated Breaker 1D72-DY-04 and 1Y52-DY-04 replacement and testing on January 28 and February 5, 2007; | |||
* Z-39 Air Dryer post-maintenance testing on February 8, 2007; | |||
* 1P-10A Residual Heat Removal pump motor MCE/EMAX and return to service on March 5, 2007; and | |||
* 1P-11A Component Cooling Water pump post-maintenance and inservice test re-baselining on March 5, 2007, following pump inner and outer bearing replacement. | |||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. | No findings of significance were identified. {{a|1R22}} | ||
{{a|1R22}} | ==1R22 Surveillance Testing== | ||
==1R22 Surveillance Testing | {{IP sample|IP=IP 71111.22}} | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
During completion of the inspection procedure samples, the inspectors | During completion of the inspection procedure samples, the inspectors observed in-plant activities and reviewed procedures and associated records to determine if: | ||
*Test equipment was used within the required range and accuracy; | * Preconditioning occurred; | ||
*Applicable prerequisites described in the test procedures were satisfied; | * Effects of the testing were adequately addressed by control room personnel or engineers prior to the commencement of the testing; | ||
*Test frequencies met TS requirements to demonstrate operability and reliability; | * Acceptance criteria were clearly stated, demonstrated operational readiness, and were consistent with the system design basis; | ||
*Tests were performed in accordance with the test procedures and | * Plant equipment calibration was correct, accurate, and properly documented; as-left setpoints were within required ranges; and the calibration frequency were in accordance with TSs, the FSAR, procedures, and applicable commitments; | ||
*Test data and results were accurate, complete, within limits, and valid; | * Measuring and test equipment calibration was current; | ||
*Test equipment was removed after testing; | * Test equipment was used within the required range and accuracy; | ||
*Where applicable for inservice testing activities, testing was performed | * Applicable prerequisites described in the test procedures were satisfied; | ||
*Unit 1 Reactor Protection and Engineered Safety Features Yellow | * Test frequencies met TS requirements to demonstrate operability and reliability; | ||
* Tests were performed in accordance with the test procedures and other applicable procedures; | |||
* Jumpers and lifted leads were controlled and restored where used; | |||
* Test data and results were accurate, complete, within limits, and valid; | |||
* Test equipment was removed after testing; | |||
* Where applicable for inservice testing activities, testing was performed in accordance with the applicable version of Section XI, American Society of Mechanical Engineers Code, and reference values were consistent with the system design basis; | |||
* Where applicable, test results not meeting acceptance criteria were addressed with an adequate operability evaluation or the system or component was declared inoperable; | |||
* Where applicable for safety-related instrument control surveillance tests, reference setting data were accurately incorporated in the test procedure; | |||
* Where applicable, actual conditions encountering high resistance electrical contacts were such that the intended safety function could still be accomplished; | |||
* Prior procedure changes had not provided an opportunity to identify problems encountered during the performance of the surveillance or calibration test; | |||
* Equipment was returned to a position or status required to support the performance of its safety functions; and | |||
* All problems identified during the testing were appropriately documented and dispositioned in the corrective action program. | |||
During this inspection period, the inspectors completed the following inspection procedure samples, which constituted two inservice tests and three routine tests, for a total of five quarterly inspection procedure samples: | |||
* Inservice testing of Service Water Pumps D, E, and F on February 21, 2007; | |||
* Unit 2 flux mapping the week of February 27, 2007; | |||
* Unit 1 Reactor Protection and Engineered Safety Features Yellow Channel Analog surveillance testing the week of February 28, 2007; | |||
* Unit 1 B Component Cooling Water Pump quarterly inservice test on March 6, 2007; and | |||
* Auxiliary Feedwater Backup Nitrogen Pressure Decay Test, P-38B during the week of March 11, 2007. | |||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. | No findings of significance were identified. {{a|1R23}} | ||
==1R23 Temporary Plant Modifications== | |||
{{IP sample|IP=IP 71111.23}} | |||
====a. Inspection Scope==== | |||
The inspectors conducted in-plant observations of physical changes to the plant and reviewed the following Temporary Modifications: | |||
* TMOD 9187, Diesel Generator Starting Air Compressor K-4B Pressure Switch PS-305A (Control Air to Lister Diesel). | |||
The review included associated work orders, temporary modification instructions/procedures, and 10 CFR 50.59 screenings. The review of the temporary modification constituted one inspection procedure sample. | |||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were | No findings of significance were identified | ||
===Cornerstone: Emergency Preparedness=== | |||
{{a|1EP6}} | |||
==1EP6 Drill Evaluation== | |||
{{IP sample|IP=IP 71114.06}} | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors observed one emergency preparedness drill evolution during | The inspectors observed one emergency preparedness drill evolution during the inspection period, observing activities in the simulator and attending the critique session. The inspectors evaluated the drill performance and determined that the critique activities appropriately captured weaknesses identified by the inspectors and verified that deficiencies were entered into the corrective action program. These activities constituted one inspection sample. | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. | No findings of significance were identified. | ||
==OTHER ACTIVITIES== | |||
{{a|4OA1}} | |||
==4OA1 Performance Indicator Verification== | |||
{{IP sample|IP=IP 71151}} | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
Cornerstones: | Cornerstones: Mitigating Systems and Barrier Integrity The inspectors reviewed the licensees recent Performance Indicator (PI)submittal, using definitions and guidance contained in Nuclear Energy Institute NEI 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 4, to assess the accuracy of the PI data. The inspectors independently re-performed calculations where applicable. The inspectors then validated the information required for each PI definition in the guideline, to determine if the licensee reported the data accurately. The following reviewed PIs constituted six inspection procedure samples: | ||
*Unplanned Downpowers.Unit 2*Unplanned Scrams;*Unplanned Scrams with Loss of Normal Heat Removal; and | Unit 1 | ||
*Unplanned Downpowers. | * Unplanned Scrams; | ||
* Unplanned Scrams with Loss of Normal Heat Removal; and | |||
* Unplanned Downpowers. | |||
Unit 2 | |||
* Unplanned Scrams; | |||
* Unplanned Scrams with Loss of Normal Heat Removal; and | |||
* Unplanned Downpowers. | |||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. | No findings of significance were identified. {{a|4OA2}} | ||
==4OA2 Identification and Resolution of Problems== | |||
{{IP sample|IP=IP 71152}} | |||
===.1 Routine Resident Inspector Review of Identification and Resolution of Problems=== | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
As discussed in previous sections of this report, the inspectors routinely reviewed | As discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to determine if issues were entered into the licensees corrective action program at an appropriate threshold, that adequate attention was given to timely corrective actions, and that adverse trends were identified and addressed. The inspectors also reviewed all CAPs written by licensee personnel during the inspection period. The CAPs written by the licensee as a result of inspectors observations are included in the list of documents in the Attachment to this report. | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified.. | No findings of significance were identified. | ||
===.2 Selected Issue Followup: Unit 2 Polar Crane Main Hoist Hook Contacted Unit 2 B=== | |||
Steam Generator Vent Line | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
This issue followup is to evaluate the | This issue followup is to evaluate the licensees corrective action program response to the issue that was self-revealed on November 14, 2006, when the Unit 2 polar crane main hook contacted the B Steam Generator vent line, as discussed in Section 4OA2 of NRC Inspection Report 05000266/2006013; 05000301/2006013. | ||
The inspection criteria for this review include: the completeness and accuracy of identification of the problem, the extent of condition, generic implications of site crane operations, classification and resolution of the issue commensurate with its safety significance, the identification of the causes of the problem, identification of corrective actions, and verification that interim corrective and compensatory actions have been identified and implemented to mitigate the effects of the problem until permanent action can be implemented. The review by the inspectors constituted one inspection procedure sample. | |||
b. Assessments and Observations The inspectors verified the adequacy of the following aspects of Condition Report AR 1061577, associated with the Unit 2 polar crane main hook contacting the B Steam Generator vent line: the completeness and accuracy of identification of the problem, the extent of condition, generic implications of site crane operations, classification and resolution of the issue commensurate with its safety significance, the identification of the causes of the problem, and the identification of corrective actions. In addition, the inspectors reviewed the licensees planned long-term corrective actions and verified their adequacy. | |||
Finally, the inspectors verified that the interim corrective actions were completed prior to the start of the Unit 1 Refueling Outage U1R30. The inspectors noted the interim corrective actions for crane moves with unloaded or bare hooks, which included a memorandum, appeared effective. However, the inspectors also noted that the long-term corrective action to revise the crane usage procedures could have been completed prior to the outage, commensurate with the potential significance of the Unit 2 incident. | |||
{{a|4OA3}} | |||
==4OA3 Event Followup== | |||
===.1 Event Notification 43149, Control Room Emergency Filtration System Declared=== | |||
Inoperable | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The Control Room Emergency Filtration System (CREFS) was declared | The Control Room Emergency Filtration System (CREFS) was declared inoperable on February 3, 2007, due to W-14B, F-16 Control Room Charcoal Filter Fan, being declared inoperable during monthly TS surveillance testing. Upon subsequent investigation of the inoperability of the W-14B fan, the W-14A fan was declared inoperable on February 6, 2007, and the appropriate 7-day TS action condition was entered. Although the subject fans were redundant, CREFS was a single train system, therefore the CREFS inoperability was reported as an event or condition that could have prevented fulfillment of a safety function and also as a degraded condition that significantly affects plant safety. The inspectors reviewed the licensees immediate response and actions taken for this event as required by 10 CFR Part 50.72. The review by the inspectors constituted one inspection procedure sample. | ||
====b. Findings==== | ====b. Findings==== | ||
=====Introduction:===== | =====Introduction:===== | ||
A non-cited violation of 10 CFR 50, Appendix B, Criterion III, | A non-cited violation of 10 CFR 50, Appendix B, Criterion III, Design Control, having very low safety significance (Green) was self-revealed on February 6, 2007, during troubleshooting of the CREFS following the breaker trip of Control Room Filter Fan W-14B on thermal overload (TOL) during surveillance testing February 3, 2007. The fan motors and breaker TOL trips were replaced in October 2006 via Modification 05-016, VNCR Emergency Fan Motor Modification. | ||
The breaker thermal overload trips were not sized appropriately for the potential range of operating conditions, nor were the breaker TOL settings tested prior to installation. | The breaker thermal overload trips were not sized appropriately for the potential range of operating conditions, nor were the breaker TOL settings tested prior to installation. | ||
Line 255: | Line 394: | ||
=====Description:===== | =====Description:===== | ||
The modification to install the new fan motors was completed and | The modification to install the new fan motors was completed and tested on October 9, 2006. The temperature during testing was approximately 50 EFahrenheit (F). During routine monthly testing of CREFS on December 8, 2006, the W-14A fan tripped. The temperature was approximately 23 EF when the fan tripped on thermal overload. The overload was replaced and the system retested successfully. Apparent Cause Evaluation ACE01066583-01 was performed and incorrectly concluded that the cause of the trip was due to infant mortality as the thermal overload relay was tripping at a value much less than design. The relay was replaced and a surveillance was subsequently performed with no failures occurring for Fan W-14A. | ||
The cause of the thermal overload trip of the W-14B fan on February 3, 2007, was evaluated by the licensee. Troubleshooting determined that the fan tripped from pumping high density cold air (approximately -11 EF) resulting in a motor current that was greater than the existing thermal overload trip settings could accommodate. (The outside air temperature was within the design parameters for the system, -15 EF to 95 EF). Applying subsequent troubleshooting results, the licensee determined that under a degraded grid condition with cold outside air temperatures, the redundant fan, W-14A could also trip with the existing TOL setting for its breaker. The change in air density from 55 EF to approximately -11 EF resulted in a calculated motor current of about 9 amperes (amps). The motor actually tripped on thermal overload at 9.2 amps. | |||
The minimum setting allows for fan operation under the worst condition of low air temperature and degraded grid and allows for a maximum of 140 percent of motor nameplate current.Analysis: | Given the accuracy of the temperature measurement, current measurement and motor cleanliness changes, the calculated trip value for the low temperature condition was close to the actual trip current measured. However, the breaker thermal overload trip at 9.2 amps was well below the 10.4 amps where the licensee anticipated breaker TOL to trip. The 10.4 amps was based on the thermal overload selected and installed for the fan motor modification. | ||
November 2, 2006, because the finding is associated with the containment barrier cornerstone of reactor safety. The inspectors evaluated the finding using IMC 0609, | |||
The reason for the lower trip value for the selected thermal overload was investigated by the licensee. The licensee determined that the relay was not tested to determine what the actual thermal overload trip point was prior to releasing the fan for use. Point Beach Nuclear Plant selects breaker TOL heaters using sizing criteria for single pole applications, but uses the heaters in a different configuration. This configuration was previously justified as satisfactory in an unreviewed and unapproved white paper that does not meet the requirements for an engineering design product. Absent a verification of the as-left trip point, PBNP has relied only on the manufacturers quality assurance program for an overload heater that operates in accordance with the published specifications. | |||
The licensee determined that the actual breaker TOL trip setpoint was required in the range of 11.5 to 12.3 amps to address the combined effects of low temperature, degraded grid conditions, and a maximum value of motor nameplate current. An engineering change, EC 10091, was issued to adjust the trip setpoint to this range. | |||
The minimum setting allows for fan operation under the worst condition of low air temperature and degraded grid and allows for a maximum of 140 percent of motor nameplate current. | |||
=====Analysis:===== | |||
The inspectors determined that the failure to address the combined affects of low ambient air temperature and degraded grid voltage for the motor thermal overload trip settings of the CREFS fan motors, in combination with an apparent inadequate methodology for determining breaker TOL settings and failure to test the breaker TOL settings, was a performance deficiency that resulted in loss of functionality of the single train CREFS and warranted a significance evaluation. | |||
The inspectors concluded that the finding is greater than minor in accordance with IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue Screening, November 2, 2006, because the finding is associated with the containment barrier cornerstone of reactor safety. The inspectors evaluated the finding using IMC 0609, Appendix A, Determining the Significance of Reactor Inspection Findings for At-Power Situations. The finding screens as (Green) very low safety significance, as it only represents a degradation of the radiological barrier function provided for the control room. The loss of CREFS fans during a release could result in increased dose to the operator in the control room potentially affecting control room habitability. Although the finding involved a potential failure of CREFS to provide its filtration function, the simultaneous occurrence of low outside temperature, degraded grid voltage and a radiological release is of very low probability. The finding for the failure to provide the correct thermal overload trip settings is a design deficiency that has a cross-cutting aspect in the area of human performance in that resources were not effective in maintaining long-term plant safety by maintenance of design margins. | |||
=====Enforcement:===== | =====Enforcement:===== | ||
10 CFR, Part 50, Appendix B, Criterion III, | 10 CFR, Part 50, Appendix B, Criterion III, Design Control, requires that the design bases are correctly translated into specifications, drawings, procedures and instructions. Contrary to these requirements, the licensee did not establish the correct thermal overload trip settings for the CREFS fan motors for MR 05-016, VNCR Emergency Fan Motor Modification, resulting in a failure to maintain sufficient design margin from the maximum expected running current to the thermal overload trip setting. | ||
As a result, CREFS Fan W-14 B tripped on thermal overload during testing with low outside ambient air temperature (approximately -11 | As a result, CREFS Fan W-14 B tripped on thermal overload during testing with low outside ambient air temperature (approximately -11 EF) and it has been shown by analysis that a trip of fan W-14A would also have been likely for the combination of low temperature and degraded grid voltage. Because this violation is of very low safety significance and has been entered into the licensees corrective action program (AR0107542), this violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy (NCV 05000266/2007002-02; 0500301/2007002-02). | ||
The licensee issued an engineering change, ECN 1601, to revise the trip setpoint to a range of 11.5 to 12.3 amps and both fans subsequently passed post maintenance and surveillance testing, restoring system operability. The licensee performed Root Cause Analysis RCE 01075472-01, Root Cause Analysis of Control Room Emergency Filter Fan System (CREFS) Motor Tripping, for these issues. The licensees planned corrective actions included the creation and implementation of a Design Guide for engineers to select new motor overload relays consistent with the National Electric Code to ensure that the design and licensing bases and the motor protection requirements were appropriately considered for modifications. The licensee also planned corrective actions to generically ensure that the initial installation testing requirements for breaker TOL trip settings are established and verified periodically. Additionally, planned corrective actions to change maintenance procedures will provide methods for setting and testing motor overload relays, consistent with the issued Design Guide. | |||
===.2 Licensee Response to Increased Frequency of Draining of the Unit 2 B Steam=== | |||
Generator Vent Line | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
On November 14, 2006, the Unit 2 polar crane main hook contacted the | On November 14, 2006, the Unit 2 polar crane main hook contacted the B Steam Generator vent line, as discussed in Section 40A3 of NRC Inspection Report 05000266/2006013; 05000301/2006013. The licensee concluded the line was operable but degraded, isolated the line with the first-off valve, 2MS-212. The licensee also implemented compensatory measures, which included periodic ultrasonic testing (UT) measurements of water level in the vent line and subsequent draining of that line, as required. Valve 2MS-212 started leaking which admitted steam/condensate into the pipe. The vent line piping downstream of the valve was to be maintained less than full to address a potential Generic Letter 96-06 overpressure concern, with 2MS-212 closed, a valve which was normally open during power operations. To maintain the line less than full, more frequent UT of the piping outside containment was required, as well as more frequent draining of the piping. In February 2007, the inspectors evaluated the stations Operational Decision-Making Issue Evaluation Document (ODMI) that addressed options to obviate the need for the frequent UT and draining of the line. | ||
The inspectors observed performance of the UT measurements, attended the | The inspectors observed performance of the UT measurements, attended the licensees working meeting to discuss the ODMI and reviewed related documentation. The inspectors concluded the licensees evaluation of options and subsequent decision to reposition the first-off isolation valve, 2MS-212, to the normal open configuration (so the entire length of the line was open back to the Steam Generator) was consistent with the station approved ODMI process and appropriate for the identified issues. Finally, the inspectors observed portions of the operations evolutions associated with the re-opening of the 2MS-212 valve. The review by the inspectors constituted one inspection procedure sample. | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. | No findings of significance were identified. | ||
{{a|4OA6}} | |||
==4OA6 Meetings== | |||
===.1 Exit Meeting=== | |||
On April 3, 2007, the resident inspectors presented the inspection results to Mr. D. Koehl and members of his staff, who acknowledged the findings. The licensee did not identify any information, provided to or reviewed by the inspectors, as proprietary. | |||
===.2 Interim Exit=== | |||
Interim exits were conducted for: | |||
* Biennial Operator Requalification Program Inspection with Mr. R. Amundson, General Supervisor Operations Training, Point Beach Nuclear Plant on January 17, 2007; and | |||
* The (Open) Unresolved Item (URI 05000266/2004010-01; 05000301/2004010-01) | |||
Operational Implementation of Alternate Shutdown Capability on January 17, 2007. | |||
ATTACHMENT: | |||
=SUPPLEMENTAL INFORMATION= | =SUPPLEMENTAL INFORMATION= | ||
Line 296: | Line 461: | ||
: [[contact::R. Johnson]], Senior Emergency Preparedness Coordinator | : [[contact::R. Johnson]], Senior Emergency Preparedness Coordinator | ||
: [[contact::T. Kendall]], Engineering Senior Technical Advisor | : [[contact::T. Kendall]], Engineering Senior Technical Advisor | ||
: [[contact::D. Koehl]], Site Vice-President | : [[contact::D. Koehl]], Site Vice-President | ||
: [[contact::G. LeClair]], Radiation Protection Supervisor | : [[contact::G. LeClair]], Radiation Protection Supervisor | ||
: [[contact::J. McCarthy]], Director of Site Operations | : [[contact::J. McCarthy]], Director of Site Operations | ||
: [[contact::J. McNamara]], Engineering Supervisor | : [[contact::J. McNamara]], Engineering Supervisor | ||
: [[contact::C. Monarch]], Fire Protection Engineer | : [[contact::C. Monarch]], Fire Protection Engineer | ||
: [[contact::R. Mrozinsky]], Appendix R Engineer | : [[contact::R. Mrozinsky]], Appendix R Engineer | ||
: [[contact::P. Nicholson]], Fire Protection Engineer | : [[contact::P. Nicholson]], Fire Protection Engineer | ||
: [[contact::G. Packard]], Plant Manager | : [[contact::G. Packard]], Plant Manager | ||
Line 310: | Line 475: | ||
: [[contact::J. Schweitzer]], Manager of Projects | : [[contact::J. Schweitzer]], Manager of Projects | ||
: [[contact::G. Sherwood]], Engineering Programs Manager | : [[contact::G. Sherwood]], Engineering Programs Manager | ||
: [[contact::C. Sizemore]], Training Manager | : [[contact::C. Sizemore]], Training Manager | ||
: [[contact::B. Vandervelde]], Maintenance Manager | : [[contact::B. Vandervelde]], Maintenance Manager | ||
: [[contact::S. Tulley]], Emergency Preparedness Manager | : [[contact::S. Tulley]], Emergency Preparedness Manager | ||
: [[contact::P. Wild]], Design Engineering Projects | : [[contact::P. Wild]], Design Engineering Projects Supervisor | ||
Nuclear Regulatory Commission | |||
: [[contact::P. Milano]], Point Beach Project Manager, NRR | : [[contact::P. Milano]], Point Beach Project Manager, NRR | ||
: [[contact::P. Louden]], Chief, Reactor Projects, Branch 5 | : [[contact::P. Louden]], Chief, Reactor Projects, Branch 5 | ||
Attachment | |||
==ITEMS OPENED, CLOSED, AND DISCUSSED== | ==ITEMS OPENED, CLOSED, AND DISCUSSED== | ||
===Closed=== | ===Opened and Closed=== | ||
05000301/2007002- | : 05000301/2007002-01 NCV Failure to Take Corrective Actions for Cold Weather Issues Prior to the Onset of Cold Weather (Section 1R01) | ||
(Section 1R01)05000266/2007002-02; | : 05000266/2007002-02; NCV Failure to Maintain Design Margin for Control Room | ||
(Section 4OA3.1) | : 05000301/2007002-02 Emergency Filtration Fan Thermal Overload Trips (Section 4OA3.1) | ||
===Discussed=== | ===Discussed=== | ||
05000266/2004010-01;05000301/2004010- | : 05000266/2004010-01; URI Operational Implementation of Alternate Shutdown | ||
: 05000301/2004010-01 Capability (Section 1R05.2) | |||
Attachment | |||
==LIST OF DOCUMENTS REVIEWED== | ==LIST OF DOCUMENTS REVIEWED== | ||
}} | }} |
Latest revision as of 09:17, 22 December 2019
ML071020081 | |
Person / Time | |
---|---|
Site: | Point Beach |
Issue date: | 04/12/2007 |
From: | Louden P NRC/RGN-III/DRP/RPB5 |
To: | Koehl D Nuclear Management Co |
References | |
IR-07-002 | |
Download: ML071020081 (33) | |
Text
ril 12, 2007
SUBJECT:
POINT BEACH NUCLEAR PLANT, UNITS 1 AND 2, NRC INTEGRATED INSPECTION REPORT 05000266/2007002 AND 05000301/2007002
Dear Mr. Koehl:
On March 31, 2007, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated inspection at your Point Beach Nuclear Plant, Units 1 and 2. The enclosed inspection report documents the inspection results, which were discussed on April 3, 2007, with you and members of your staff.
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations, and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed your personnel.
Based on the results of this inspection, two findings of very low safety significance associated with violations of NRC requirements were identified. However, because of the very low safety significance and because they are entered into your corrective action program, the NRC is treating these findings as non-cited violations (NCVs) consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest any NCV in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with copies to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector at the Point Beach Nuclear Plant. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records System (PARS)
component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA/
Patrick L. Louden, Chief Branch 5 Division of Reactor Projects Docket Nos. 50-266; 50-301 License Nos. DPR-24; DPR-27 Enclosure: Inspection Report 05000266/2007002; 05000301/2007002 w/Attachment: Supplemental Information cc w/encl: F. Kuester, President and Chief Executive Officer, We Generation D. Cooper, Senior Vice President and Chief Nuclear Officer J. McCarthy, Site Director of Operations D. Weaver, Nuclear Asset Manager Plant Manager Regulatory Affairs Manager Training Manager Site Assessment Manager Site Engineering Director Emergency Planning Manager J. Rogoff, Vice President, Counsel & Secretary K. Duveneck, Town Chairman Town of Two Creeks Chairperson Public Service Commission of Wisconsin J. Kitsembel, Electric Division Public Service Commission of Wisconsin State Liaison Officer
SUMMARY OF FINDINGS
IR 05000266/2007002 and 05000301/2007002; 01/01/2007 - 03/31/2007; Point Beach Nuclear
Plant, Units 1 and 2; Adverse Weather Protection; and Event Followup.
This report covers a 3-month period of inspections by resident inspectors and regional specialists. Two Green findings with associated non-cited violations were identified. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.
A. Inspector-Identified and Self-Revealed Findings
Cornerstone: Initiating Events
- Green.
The inspectors identified a finding and associated non-cited violation (NCV) of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, having very low safety significance (Green) for the failure to take prompt corrective actions to address a potential cold weather issue initially identified in October 2006 and again in January 2007. The failure to take prompt corrective actions led to the formation of ice on offsite power and plant equipment cable trays and cabling. The sheets of ice were also in close proximity to the Unit 2 Refueling Water Storage Tank level indicators and outlet piping. The licensee initiated condition reports and took immediate corrective actions and had planned additional corrective actions based on a causal evaluation.
The finding is greater than minor because if left uncorrected the finding would become a more significant safety concern in that the formation of ice in the facade building in this case could have affected safety-related equipment. In addition, the finding is associated with the external factors attribute of the Initiating Events cornerstone and affected the cornerstone objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Because the significant ice buildup in the Unit 2 facade was an external factor and transient initiator contributor, and did not contribute to both the likelihood of both a reactor trip and that mitigation equipment or functions would not be available, the finding is considered to be of very low safety significance (Green). This finding has a cross-cutting aspect in the area of problem identification and resolution because the licensee did not take appropriate corrective actions in a timely manner, commensurate with their safety significance and complexity. (Section 1R01)
Cornerstone: Barrier Integrity
- Green: A non-cited violation (NCV) of 10 CFR 50, Appendix B, Criterion III,
Design Control, having very low safety significance was self-revealed for the failure to maintain sufficient design margin for the expected running currents of the control room emergency filtration system fans to their thermal overload trip settings. This occurred due to design errors in a modification that replaced the fans in October 2006. Control Room Emergency Filtration System (CREFS)
Fan W-1-B tripped on a breaker thermal overload during surveillance testing in February 2007 with low outside ambient air temperature (approximately negative 11EFahrenheit). Licensee analyses also demonstrated that a trip of fan W-14A could have occurred for the combination of low ambient temperature and degraded grid voltage. The licensee took immediate corrective actions to replace the breaker thermal overloads with thermal overloads of a higher setting as a result of troubleshooting and evaluations performed following the trip of the W-14B fan. The issue was entered into the licensees corrective action program and a root cause evaluation was subsequently performed.
The finding is greater than minor because it is associated with the attribute of maintaining radiological barrier functionality of the control room and affected the Barrier Integrity cornerstone objective to provide reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events. Loss of CREFS fans during a release could result in increased dose to the operators in the control room potentially affecting control room habitability. Although the finding involved a potential failure of the CREFS to provide its filtration function, the simultaneous occurrence of low outside air temperature, degraded grid voltage, and a radiological release is of very low probability. The finding for the failure to provide the correct thermal overload trip setting is a design deficiency that has a cross-cutting aspect in the area of human performance in that resources were not effective in maintaining long-term plant safety by maintenance of design margins. (Section 4OA3)
REPORT DETAILS
Summary of Plant Status
Unit 1 was at 100 percent power throughout the inspection period with the exception of brief downpowers during routine auxiliary feedwater and secondary system valve testing and until March 31, 2007, when the unit was shutdown to commence U1R30 refueling outage.
Unit 2 was at 100 percent power throughout the inspection period with the exception of brief downpowers during routine auxiliary feedwater and secondary system valve testing.
REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
1R01 Adverse Weather Protection
a. Inspection Scope
The inspectors walked down accessible portions of risk-significant equipment and systems susceptible to cold weather freezing during the onset of cold weather. The inspectors walked down all accessible portions of the Units 1 and 2 facade buildings, which enclosed the reactor containments and certain plant equipment inside the protected area. The inspectors reviewed the corrective actions and work orders (WOs)written to correct identified problems. The inspectors also walked down areas which had a history of freeze problems. This observation constituted one inspection procedure system sample.
b. Findings
Introduction:
The inspectors identified a finding and associated non-cited violation (NCV) of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, having very low safety significance (Green) for the failure to take prompt corrective actions to address a potential cold weather issue initially identified in October 2006 and again in January 2007. The failure to take prompt corrective actions led to the formation of ice on offsite power and plant equipment cable trays and cabling. The sheets of ice were also in close proximity to the Unit 2 Refueling Water Storage Tank (RWST) level indicators and outlet piping.
Description:
On February 6, 2007, plant staff identified that in the Unit 2 containment facade a wall of ice had formed on cable trays and portions of cabling within the trays.
The containment facade is an unheated structure surrounding the containment building which contains some plant electrical equipment and other various safety-related equipment, such as the RWST. The cable trays contained the offsite power lines from a Unit 2 transformer to the associated busses, in addition to various equipment cabling.
The ice had formed on either side of the cable tray, and had a maximum dimension on one side of the cable tray of approximately 15 feet high by 6 feet wide and a thickness of greater than 1 inch. Operations staff immediately requested walkdowns from system and structural engineers to determine the structural acceptability of the trays current state which were judged satisfactory. The ice wall and cable trays were approximately 5 feet away from the RWST and near the outlet piping for the RWST, the inlet for the RWST minimum flow recirculation piping, and the level transmitters for the RWST.
Operations directed maintenance craft to create a tent with a temporary heat source to melt the ice and redirect the source of water.
On February 7, 2007, the inspectors walked down the Unit 2 facade and questioned whether: the melting icicles presented a threat to the equipment below; certain junction boxes covered in ice would be affected by the water as the ice was melted; and certain portions of the facade freeze system were in jeopardy of not functioning due to the melting ice. Operations and engineering determined that no adverse conditions existed and additional operator walkdowns were performed of the facade freeze system (which prevents safety-related lines from freezing during cold weather) and area. The licensee also determined the source of the water was a leaking steam relief valve in the radioactive waste system. The relief valve was located on the 46-foot elevation of the facade and the steam normally relieved into the Primary Auxiliary Building Relief Stack located adjacent to the RWST. The licensee continued with actions to melt the ice on the trays, monitor the area and redirect the water. Finally, the inspectors noted that Condition Report AR0107430, written in January 2007, identified the leaking relief valve and stated that the issue would be a problem when colder weather arrived. The inspectors also identified to the licensee that the condition report appeared to have been inadvertently closed 1 week prior with no actions taken. Finally, the inspectors learned from discussions with plant staff that this area had experienced ice formation in prior years, although no corrective action documentation was found.
On February 8, 2007, the inspectors again walked down the facade and concluded that the relief vent stack, approximately 20 inches in diameter, was most likely filled with a combination of ice and water and noted that the licensee still had not taken any action to address the source of the leak. The inspectors also questioned whether the licensee had considered the potential adverse affects of the relief stack, likely filled with ice and water to a height of approximately 40 feet, near the Unit 2 RWST. The licensee performed additional evaluations to provide reasonable assurance that the vent line would remain intact during a seismic event and initiated actions to thaw the frozen relief stack drain. The thawing of the relief vent stack drain resulted in the sudden removal of a large volume of water from the relief vent stack, along with the melting of ice within the relief stack. In addition, the licensee took immediate corrective actions to replace the leaking relief valve to isolate the source of water.
The licensee subsequently performed an apparent cause evaluation and identified that a second Condition Report, AR01054609, was written in October 2006 identifying the leaking relief valve and the fact this would become a cold weather issue. The condition report was closed to a work request at that time, and neither the condition report, nor the work request were flagged in the licensees work order and corrective action systems as a cold weather issue. The January 2007 condition report was also not flagged as a cold weather issue and was inadvertently closed due to an inadequate communication. Therefore, multiple barriers, including the corrective action program screening team and work request screening team, failed to identify and track this cold weather issue. The licensee also determined the relief valve vent stack drain froze due to abandonment of the heat trace circuit during the facade freeze heat trace upgrade project in 1999. The licensee subsequently determined as a result of the extent of condition that an additional 40 circuits were abandoned in 1999 with no documentation justifying that action. Finally, as a result of increased attention in this area, the licensee identified an additional 5 facade cold weather issues, which were addressed.
Analysis:
The inspectors determined that the licensees failure to implement prompt corrective actions to correct equipment deficiencies prior to the onset of cold weather, which could have significantly impacted safety-related equipment, was a performance deficiency requiring a significance evaluation. Using IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue Screening, dated November 2, 2006, the inspectors concluded that the finding is greater than minor because if left uncorrected the finding would become a more significant safety concern in that the formation of ice in the facade building in this case could have affected safety-related equipment. In addition, the finding is associated with the external factors attribute of the Initiating Events cornerstone and affected the cornerstone objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during shutdown as well as power operations.
The inspectors evaluated the finding using IMC 0609, Significance Determination Process, Appendix A, Determining the Significance of Reactor Inspection Findings for At-Power Situations, dated November 22, 2005. The transient initiator contributor was the external factor of significant ice buildup in the Unit 2 facade, and did not contribute to both the likelihood of both a reactor trip and that mitigation equipment or functions would not be available. Consequently, the finding is considered to be of very low safety significance (Green).
The inspectors also determined that a primary cause of this finding is related to the cross-cutting area of problem identification and resolution. Specifically, under the component of corrective action program, the licensee failed to ensure the aspect of taking appropriate corrective actions to address safety issues in a timely manner, which directly contributed to this performance deficiency.
Enforcement:
10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, states, in part, that measures shall be established to assure that conditions adverse to quality, such as deficiencies, deviations, and nonconformances, are promptly identified and corrected. Contrary to this, the licensee was made aware of a condition adverse to quality associated with the leaking relief valve on two occasions in October 2006 and January 2007 and did not take prompt corrective actions to correct the condition prior to the onset of cold weather and potential impacts on safety-related systems. The failure to implement prompt corrective actions for these conditions adverse to quality is a violation of 10 CFR Part 50, Appendix B, Criterion XVI. Because of the very low safety significance of this finding and because the issue was entered into the licensees corrective action program (AR01075828), it is being treated as an NCV, consistent with Section VI.A.1 of the Enforcement Policy (NCV 05000301/2007002-01).
As stated previously, the licensee took corrective actions to correct the condition upon discovery and performed an apparent cause evaluation. Additional actions taken to address the apparent cause that the corrective action and work request screening teams failed to properly classify work request and condition reports as cold weather issues and subsequently assign timely corrective actions included: actions to both teams to review the event and procedure expectations regarding assigning the proper attributes for any condition to condition reports and work requests; an informational bulletin was sent to plant personnel to ensure the appropriate attributes are contained on work requests; operations staff reviewed the event and reinforced expectations regarding log entries, turnover information, and documentation of condition reports; the 40 abandoned circuits were evaluated to determine which require re-energization; re-energization of the relief valve vent stack facade freeze protection circuit; determination whether the RWST vent lines require freeze protection; and determination if any configuration changes were required for sample and drain locations in the facades.
1R04 Equipment Alignment
.1 Partial System Walkdowns
a. Inspection Scope
The inspectors performed partial walkdowns of accessible portions of risk-significant systems to determine the operability of the systems. The inspectors utilized system valve lineup and electrical breaker checklists, tank level books, plant drawings, and selected operating procedures to determine if the systems were correctly aligned to perform the intended design functions. The inspectors also examined the material condition of the components and observed operating equipment parameters to determine whether deficiencies existed. The inspectors reviewed completed work orders (WOs) and calibration records associated with the systems for issues that could affect component or train functions. The inspectors used the information in the appropriate sections of the Final Safety Analysis Report (FSAR) to determine the functional requirements of the system. Partial system walkdowns of the following systems constituted three inspection procedure samples:
- Service Water Trains A, B, and C;
- Service Water Trains D, E, and F; and
- Unit 1 Component Cooling Water (CCW).
b. Findings
No findings of significance were identified.
.2 Complete System Walkdowns
a. Inspection Scope
The inspectors performed a complete system alignment inspection of the Auxiliary Feedwater (AFW) system for Units 1 and 2. This safety-related system was selected based on the risk-significance of the system in the licensees probabilistic risk assessment. The walkdown of the AFW constituted one semiannual inspection procedure sample.
The inspection consisted of the following activities:
- Review of plant procedures (including selected abnormal and emergency procedures), drawings, and the FSAR to identify proper system alignment;
- Review of outstanding or completed temporary and permanent modifications to the system;
- Review of open corrective action program documents (CAP ARs) and WOs that could impact operability of the system; and
- Walkdown of mechanical and electrical components in the system to assess alignment, component accessibility, availability, and current condition.
b. Findings
No findings of significance were identified.
1R05 Fire Protection
.1 Walkdown of Selected Fire Zones
a. Inspection Scope
The inspectors conducted fire protection walkdowns which focused on the following attributes: the availability, accessibility, and condition of fire fighting equipment; the control of transient combustibles and ignition sources; and the condition and status of installed fire barriers. The inspectors selected fire areas for inspection based on the areas overall fire risk contribution, as documented in the Individual Plant Examination of External Events, or the potential of a fire to impact equipment that could initiate a plant transient.
In addition, the inspectors assessed these additional fire protection attributes during walkdowns: fire hoses and extinguishers were in the designated locations and available for immediate use; unobstructed fire detectors and sprinklers; transient material loading within the analyzed limits; and fire doors, dampers, and penetration seals in satisfactory condition. The inspectors also determined if minor issues identified during the inspection were entered into the licensees corrective action program. The walkdown of the following selected fire zones constituted eight inspection procedure samples:
- Fire Zone FZ596/Fire Area A01-H; Unit 2 Containment Facade;
- Fire Zone 156/Fire Area A06; MCC 1B32 and Fire Zone 154/Fire Area A05; Charging Pump 1P2A;
- Fire Zone 166/Fire Area A15; MCC 2B32 and Fire Zone 155/Fire Area A05; Charging Pump 2P2A;
- Fire Zone 152/Fire Area A03; Charging Pump 1P2C;
- Fire Zone 153/Fire Area A04; Charging Pump 1P2B;
- Fire Zone 163/Fire Area A12; Charging Pump 2P2C;
- Fire Zone 164/Fire Area A13; Charging Pump 1P2B; and
- Fire Zone 771/Fire Area A61; Fuel Oil Pump Room.
b. Findings
No findings of significance were identified.
.2 (Open) Unresolved Item (URI 05000266/2004010-01; 05000301/2004010-01) -
Operational Implementation of Alternate Shutdown Capability The Point Beach Nuclear Plant (PBNP) Fire Protection Program (FPP) described the means by which safe shutdown could be achieved to meet the requirements of 10 CFR Part 50, Appendix R, Sections III.G.3 and III.L. The PBNP safe shutdown analysis identified the minimum number of components and plant systems necessary for achieving Appendix R safe shutdown performance goals. The FPP accomplished safe shutdown by isolating power to most plant equipment and then used an emergency diesel generator or the station blackout turbine generator to power equipment necessary for plant shutdown. Numerous manual actions were required with four operations staff working together to shutdown both Unit 1 and Unit 2.
a. Inspection Scope
The inspectors performed a review of licensee actions regarding URI 05000266/2004010-01; 05000301/2004010-01. This URI was associated with a lack of time for critical manual actions in Abnormal Operating Procedure (AOP) AOP-10A, Safe Shutdown - Local Control, Revision 39, and AOP 10C, Safe Shutdown Following a Fire at PAB [Primary Auxiliary Building] 26 Foot Central, Revision 0. The fire protection procedures were common to both units and were to be implemented as fire area specific (i.e., alternate shutdown (ASD))
procedures for the Control Room, Cable Spreading Room, and the 26-foot elevation of the PAB. The inspectors reviewed the licensees evaluation for these procedures.
In addition, the inspectors reviewed the licensee actions regarding Fire Operating Procedure (FOP) 1.2, Potential Fire Affected Safe Shutdown Equipment, Revision 15, which had not previously identified time critical manual actions for plant fire scenarios.
The inspectors reviewed the licensees evaluation for time critical manual actions and changes to this procedure.
Description:
The URI issue for procedures AOP-10 and FOP 1.2 regarded the potential for not having adequate water inventory available for reactor makeup during the 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> required to reach cold shutdown because of Reactor Coolant Pump (RCP) leakage and the potential drain down of the RWST (i.e., through a spuriously operated valve to the containment sump) from an Appendix R Fire. As a result, the inspectors were concerned that the licensee had the potential for a non-conservative Appendix R manual action response time in their procedures for ensuring that the RWST was isolated from draining to the containment.
The licensee initiated a CAP to formalize a previously unapproved evaluation and prepare a new calculation for the AOP-10 manual actions. The licensee entered this issue into their corrective action program as CAP060624, Potentially Non-Conservative Appendix R Response Times, dated November 18, 2004. The licensee completed a review and performed a new calculation to resolve the AOP issue. The licensee performed Calculation WE00010-05, Revision 0, which indicated that adequate time existed to close RWST valves to the containment and maintain an adequate inventory of water in the RWST. The inspectors reviewed this calculation and verified that adequate time existed to isolate the valves to containment and ensure a safe shutdown of the plant. This portion of the URI is considered closed.
The inspectors had identified a similar issue where the licensee did not identify the time critical manual actions in FOP 1.2, Potential Fire Affected Safe Shutdown Equipment, Revision 6. However, unlike the AOP-10 procedures, with step by step operator actions to shut down the plant, these procedures were symptom-based, making it difficult to identify a spurious actuation and take a manual action. For example, fires in certain fire areas required time critical manual actions, to ensure that the RWST is isolated to prevent drain down of water to the containment sump. As a result of the inspectors concern, the licensee issued CAP 060641, FOP 1.2 Enhancement Recommendation, November 19, 2004, to review this issue. During the resolution of this issue, the licensee initiated compensatory actions, such as, assigning hourly fire rounds for all areas where a fire could potential cause a spurious actuation and a subsequent drain down of the RWST. The licensees corrective actions included identifying time critical manual actions in this procedure and then prioritizing those manual actions that needed to be performed early during fire scenarios.
However, the inspectors noted that the licensee took credit in its evaluation for a third valve (Valve 1/2SI 851 A/B) with an unknown leakage rate in the RWST piping. In addition, the licensee had not identified the location of the control circuitry, torque, and limit switch wiring for this valve nor evaluated fire scenarios for this wiring. Additionally, the licensee used only a single spurious actuation per fire to resolve this issue.
Reliance upon a single spurious actuation was inconsistent with the licensees Safe Shutdown Analysis Report (SSAR) and Fire Protection Evaluation Report (FPER). The use of a single spurious actuation per fire area during fire scenarios is an issue that continues to be evaluated by the NRC. As a result, this portion of the URI remains open pending regulatory resolution of the fire protection circuits generic issue.
b. Findings
No findings of significance were identified.
1R11 Licensed Operator Requalification
.1 Resident Inspector Quarterly Observation of Licensed Operator Requalification
a. Inspection Scope
On February 15, 2007, the inspectors observed the operating crew performance during a simulator as-found requalification examination. Observation of the requalification quarterly evaluation constituted one inspection procedure sample.
The inspectors assessed crew performance in the areas of:
- Clarity and formality of communications;
- Understanding of the interactions and function of the operating crew during an emergency;
- Prioritization, interpretation, and verification of actions required for emergency procedure use and interpretation;
- Oversight and direction from supervisors; and
- Group dynamics.
Crew performance in these areas was also compared to licensee management expectations and guidelines, as presented in nuclear plant procedure NP 2.1.1, Conduct of Operations. The inspectors also verified that the licensee and crew assessed and critiqued crew performance accordingly.
b. Findings
No findings of significance were identified.
.2 Operating Test Results
a. Inspection Scope
The inspectors reviewed the overall pass/fail results of the comprehensive annual job performance measure operating tests, the annual simulator operating tests, and the biennial written examinations (required to be given per 10 CFR 55.59(a)(2)). The operating tests were administered by the licensee from August through October 2006.
The written examinations were conducted during December 2006. The overall results were compared with the significance determination process in accordance with NRC Manual Chapter 0609, Appendix I, Operator Requalification Human Performance Significance Determination Process (SDP).
b. Findings
No findings of significance were identified.
1R12 Maintenance Effectiveness
a. Inspection Scope
The inspectors performed maintenance effectiveness reviews of the systems listed below. The inspectors reviewed repetitive maintenance activities to assess maintenance effectiveness, including maintenance rule activities, work practices, and common cause issues. Inspection activities included, but were not limited to, the licensee's categorization of specific issues, including evaluation of performance criteria, appropriate work practices, identification of common cause errors, extent of condition, and trending of key parameters. Additionally, the inspectors reviewed implementation of the Maintenance Rule (10 CFR 50.65) requirements, including a review of scoping, goal-setting, performance monitoring, short-term and long-term corrective actions, functional failure determinations, and current equipment performance status.
For each system reviewed, the inspectors reviewed significant WOs and CAPs to determine if failures were appropriately identified, classified, and corrected, and if unavailable time was correctly calculated. The reviews of maintenance effectiveness for the following components and systems constituted two inspection procedure samples:
- 125-V DC Safety-Related Battery Chargers, D-07, D-08, D-09, D-107, D-108 and D-109; and
- 125-V DC Safety-Related Batteries D-05, D-06, D-105, D-106, and D-305.
b. Findings
No findings of significance were identified.
1R13 Maintenance Risk Assessment and Emergent Work Evaluation
a. Inspection Scope
The inspectors reviewed risk assessments for planned and emergent maintenance activities during the specified work weeks. During these reviews, the inspectors compared the licensees risk management actions to those actions specified in the licensees procedures for the assessment and management of risk associated with maintenance activities. The inspectors assessed whether evaluation, planning, control, and performance of the work were done in a manner to reduce the risk and minimize the duration where practical, and whether contingency plans were in place where appropriate.
The inspectors used the licensees daily configuration risk assessment records, observations of shift turnover meetings, and observations of daily plant status meetings to determine if the equipment configurations were properly listed. The inspectors also verified that protected equipment was identified and controlled as appropriate, and that significant aspects of plant risk were communicated to the necessary personnel. The reviews of maintenance risk assessment and emergent work evaluation constituted seven inspection procedure samples:
- Planned and emergent maintenance during the week of January 21, 2007;
- Planned and emergent maintenance during the week of February 4, 2007;
- Planned and emergent maintenance during the week of February 12, 2007;
- Planned and emergent maintenance during the week of February 18,2007;
- Planned and emergent maintenance during the week of March 4, 2007;
- Planned and emergent maintenance during the week of March 11, 2007; and
- Planned and emergent maintenance during the week of March 26, 2007.
b. Findings
No findings of significance were identified.
1R15 Operability Evaluations
a. Inspection Scope
The inspectors reviewed selected operability evaluations (OPRs) associated with issues entered into the licensees corrective action program. The inspectors reviewed design basis information, the FSAR, Technical Specification (TS) requirements, and licensee procedures to determine the technical adequacy of the operability evaluations. In addition, the inspectors determined if compensatory measures were implemented, as required. The inspectors assessed whether system operability was properly justified and that the system remained available, such that no unrecognized increase in risk occurred. The reviews of the following operability evaluations constituted four procedure samples:
- OBD for AR1043614, Battery D-06 Decreasing Specific Gravity Trends;
- AR1075828, Operability Assessment for Facade Freezing; and
- AR1068922, Issues with CCW Containment Penetrations Unit 1 P-20 &
Unit 2 P-19.
b. Findings
No findings of significance were identified.
1R19 Post-Maintenance Testing
a. Inspection Scope
During completion of the post-maintenance test inspection procedure samples, the inspectors observed in-plant activities and reviewed procedures and associated records to determine if:
- Testing activities satisfied the test procedure acceptance criteria;
- Effects of the testing were adequately addressed prior to the testing;
- Measuring and test equipment calibration was current;
- Test equipment was within the required range and accuracy;
- Applicable prerequisites described in the test procedures were satisfied;
- Affected systems or components were removed from service in accordance with approved procedures;
- Testing activities were performed in accordance with the test procedures and other applicable procedures;
- Jumpers and lifted leads were controlled and restored where used;
- Test data and results were accurate, complete, and valid;
- Test equipment was removed after testing;
- Equipment was returned to a position or status required to support the operability of the system in accordance with approved procedures; and
- All problems identified during the testing were appropriately entered into the corrective action program.
The activities listed below were reviewed by the inspectors and constituted seven quarterly inspection procedure samples:
- Emergency Diesel Generator G-03 Governor testing on January 9, 2007;
- Emergency Diesel Generator G-03 Governor testing on January 11, 2007;
- Unit 1 Containment Spray Inservice Test of Pumps and Valves on January 17,2007;
- Unit 1 Manually Operated Breaker 1D72-DY-04 and 1Y52-DY-04 replacement and testing on January 28 and February 5, 2007;
- Z-39 Air Dryer post-maintenance testing on February 8, 2007;
- 1P-10A Residual Heat Removal pump motor MCE/EMAX and return to service on March 5, 2007; and
- 1P-11A Component Cooling Water pump post-maintenance and inservice test re-baselining on March 5, 2007, following pump inner and outer bearing replacement.
b. Findings
No findings of significance were identified.
1R22 Surveillance Testing
a. Inspection Scope
During completion of the inspection procedure samples, the inspectors observed in-plant activities and reviewed procedures and associated records to determine if:
- Preconditioning occurred;
- Effects of the testing were adequately addressed by control room personnel or engineers prior to the commencement of the testing;
- Acceptance criteria were clearly stated, demonstrated operational readiness, and were consistent with the system design basis;
- Plant equipment calibration was correct, accurate, and properly documented; as-left setpoints were within required ranges; and the calibration frequency were in accordance with TSs, the FSAR, procedures, and applicable commitments;
- Measuring and test equipment calibration was current;
- Test equipment was used within the required range and accuracy;
- Applicable prerequisites described in the test procedures were satisfied;
- Test frequencies met TS requirements to demonstrate operability and reliability;
- Tests were performed in accordance with the test procedures and other applicable procedures;
- Jumpers and lifted leads were controlled and restored where used;
- Test data and results were accurate, complete, within limits, and valid;
- Test equipment was removed after testing;
- Where applicable for inservice testing activities, testing was performed in accordance with the applicable version of Section XI, American Society of Mechanical Engineers Code, and reference values were consistent with the system design basis;
- Where applicable, test results not meeting acceptance criteria were addressed with an adequate operability evaluation or the system or component was declared inoperable;
- Where applicable for safety-related instrument control surveillance tests, reference setting data were accurately incorporated in the test procedure;
- Where applicable, actual conditions encountering high resistance electrical contacts were such that the intended safety function could still be accomplished;
- Prior procedure changes had not provided an opportunity to identify problems encountered during the performance of the surveillance or calibration test;
- Equipment was returned to a position or status required to support the performance of its safety functions; and
- All problems identified during the testing were appropriately documented and dispositioned in the corrective action program.
During this inspection period, the inspectors completed the following inspection procedure samples, which constituted two inservice tests and three routine tests, for a total of five quarterly inspection procedure samples:
- Inservice testing of Service Water Pumps D, E, and F on February 21, 2007;
- Unit 2 flux mapping the week of February 27, 2007;
- Unit 1 Reactor Protection and Engineered Safety Features Yellow Channel Analog surveillance testing the week of February 28, 2007;
- Unit 1 B Component Cooling Water Pump quarterly inservice test on March 6, 2007; and
- Auxiliary Feedwater Backup Nitrogen Pressure Decay Test, P-38B during the week of March 11, 2007.
b. Findings
No findings of significance were identified.
1R23 Temporary Plant Modifications
a. Inspection Scope
The inspectors conducted in-plant observations of physical changes to the plant and reviewed the following Temporary Modifications:
- TMOD 9187, Diesel Generator Starting Air Compressor K-4B Pressure Switch PS-305A (Control Air to Lister Diesel).
The review included associated work orders, temporary modification instructions/procedures, and 10 CFR 50.59 screenings. The review of the temporary modification constituted one inspection procedure sample.
b. Findings
No findings of significance were identified
Cornerstone: Emergency Preparedness
1EP6 Drill Evaluation
a. Inspection Scope
The inspectors observed one emergency preparedness drill evolution during the inspection period, observing activities in the simulator and attending the critique session. The inspectors evaluated the drill performance and determined that the critique activities appropriately captured weaknesses identified by the inspectors and verified that deficiencies were entered into the corrective action program. These activities constituted one inspection sample.
b. Findings
No findings of significance were identified.
OTHER ACTIVITIES
4OA1 Performance Indicator Verification
a. Inspection Scope
Cornerstones: Mitigating Systems and Barrier Integrity The inspectors reviewed the licensees recent Performance Indicator (PI)submittal, using definitions and guidance contained in Nuclear Energy Institute NEI 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 4, to assess the accuracy of the PI data. The inspectors independently re-performed calculations where applicable. The inspectors then validated the information required for each PI definition in the guideline, to determine if the licensee reported the data accurately. The following reviewed PIs constituted six inspection procedure samples:
Unit 1
- Unplanned Scrams;
- Unplanned Scrams with Loss of Normal Heat Removal; and
- Unplanned Downpowers.
Unit 2
- Unplanned Scrams;
- Unplanned Scrams with Loss of Normal Heat Removal; and
- Unplanned Downpowers.
b. Findings
No findings of significance were identified.
4OA2 Identification and Resolution of Problems
.1 Routine Resident Inspector Review of Identification and Resolution of Problems
a. Inspection Scope
As discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to determine if issues were entered into the licensees corrective action program at an appropriate threshold, that adequate attention was given to timely corrective actions, and that adverse trends were identified and addressed. The inspectors also reviewed all CAPs written by licensee personnel during the inspection period. The CAPs written by the licensee as a result of inspectors observations are included in the list of documents in the Attachment to this report.
b. Findings
No findings of significance were identified.
.2 Selected Issue Followup: Unit 2 Polar Crane Main Hoist Hook Contacted Unit 2 B
Steam Generator Vent Line
a. Inspection Scope
This issue followup is to evaluate the licensees corrective action program response to the issue that was self-revealed on November 14, 2006, when the Unit 2 polar crane main hook contacted the B Steam Generator vent line, as discussed in Section 4OA2 of NRC Inspection Report 05000266/2006013; 05000301/2006013.
The inspection criteria for this review include: the completeness and accuracy of identification of the problem, the extent of condition, generic implications of site crane operations, classification and resolution of the issue commensurate with its safety significance, the identification of the causes of the problem, identification of corrective actions, and verification that interim corrective and compensatory actions have been identified and implemented to mitigate the effects of the problem until permanent action can be implemented. The review by the inspectors constituted one inspection procedure sample.
b. Assessments and Observations The inspectors verified the adequacy of the following aspects of Condition Report AR 1061577, associated with the Unit 2 polar crane main hook contacting the B Steam Generator vent line: the completeness and accuracy of identification of the problem, the extent of condition, generic implications of site crane operations, classification and resolution of the issue commensurate with its safety significance, the identification of the causes of the problem, and the identification of corrective actions. In addition, the inspectors reviewed the licensees planned long-term corrective actions and verified their adequacy.
Finally, the inspectors verified that the interim corrective actions were completed prior to the start of the Unit 1 Refueling Outage U1R30. The inspectors noted the interim corrective actions for crane moves with unloaded or bare hooks, which included a memorandum, appeared effective. However, the inspectors also noted that the long-term corrective action to revise the crane usage procedures could have been completed prior to the outage, commensurate with the potential significance of the Unit 2 incident.
4OA3 Event Followup
.1 Event Notification 43149, Control Room Emergency Filtration System Declared
a. Inspection Scope
The Control Room Emergency Filtration System (CREFS) was declared inoperable on February 3, 2007, due to W-14B, F-16 Control Room Charcoal Filter Fan, being declared inoperable during monthly TS surveillance testing. Upon subsequent investigation of the inoperability of the W-14B fan, the W-14A fan was declared inoperable on February 6, 2007, and the appropriate 7-day TS action condition was entered. Although the subject fans were redundant, CREFS was a single train system, therefore the CREFS inoperability was reported as an event or condition that could have prevented fulfillment of a safety function and also as a degraded condition that significantly affects plant safety. The inspectors reviewed the licensees immediate response and actions taken for this event as required by 10 CFR Part 50.72. The review by the inspectors constituted one inspection procedure sample.
b. Findings
Introduction:
A non-cited violation of 10 CFR 50, Appendix B, Criterion III, Design Control, having very low safety significance (Green) was self-revealed on February 6, 2007, during troubleshooting of the CREFS following the breaker trip of Control Room Filter Fan W-14B on thermal overload (TOL) during surveillance testing February 3, 2007. The fan motors and breaker TOL trips were replaced in October 2006 via Modification 05-016, VNCR Emergency Fan Motor Modification.
The breaker thermal overload trips were not sized appropriately for the potential range of operating conditions, nor were the breaker TOL settings tested prior to installation.
The purpose of the modification was to add margin to the measured makeup air flow rate for the emergency fans as the CREFS had only marginally passed a previous TS Surveillance 3.7.9.6.
Description:
The modification to install the new fan motors was completed and tested on October 9, 2006. The temperature during testing was approximately 50 EFahrenheit (F). During routine monthly testing of CREFS on December 8, 2006, the W-14A fan tripped. The temperature was approximately 23 EF when the fan tripped on thermal overload. The overload was replaced and the system retested successfully. Apparent Cause Evaluation ACE01066583-01 was performed and incorrectly concluded that the cause of the trip was due to infant mortality as the thermal overload relay was tripping at a value much less than design. The relay was replaced and a surveillance was subsequently performed with no failures occurring for Fan W-14A.
The cause of the thermal overload trip of the W-14B fan on February 3, 2007, was evaluated by the licensee. Troubleshooting determined that the fan tripped from pumping high density cold air (approximately -11 EF) resulting in a motor current that was greater than the existing thermal overload trip settings could accommodate. (The outside air temperature was within the design parameters for the system, -15 EF to 95 EF). Applying subsequent troubleshooting results, the licensee determined that under a degraded grid condition with cold outside air temperatures, the redundant fan, W-14A could also trip with the existing TOL setting for its breaker. The change in air density from 55 EF to approximately -11 EF resulted in a calculated motor current of about 9 amperes (amps). The motor actually tripped on thermal overload at 9.2 amps.
Given the accuracy of the temperature measurement, current measurement and motor cleanliness changes, the calculated trip value for the low temperature condition was close to the actual trip current measured. However, the breaker thermal overload trip at 9.2 amps was well below the 10.4 amps where the licensee anticipated breaker TOL to trip. The 10.4 amps was based on the thermal overload selected and installed for the fan motor modification.
The reason for the lower trip value for the selected thermal overload was investigated by the licensee. The licensee determined that the relay was not tested to determine what the actual thermal overload trip point was prior to releasing the fan for use. Point Beach Nuclear Plant selects breaker TOL heaters using sizing criteria for single pole applications, but uses the heaters in a different configuration. This configuration was previously justified as satisfactory in an unreviewed and unapproved white paper that does not meet the requirements for an engineering design product. Absent a verification of the as-left trip point, PBNP has relied only on the manufacturers quality assurance program for an overload heater that operates in accordance with the published specifications.
The licensee determined that the actual breaker TOL trip setpoint was required in the range of 11.5 to 12.3 amps to address the combined effects of low temperature, degraded grid conditions, and a maximum value of motor nameplate current. An engineering change, EC 10091, was issued to adjust the trip setpoint to this range.
The minimum setting allows for fan operation under the worst condition of low air temperature and degraded grid and allows for a maximum of 140 percent of motor nameplate current.
Analysis:
The inspectors determined that the failure to address the combined affects of low ambient air temperature and degraded grid voltage for the motor thermal overload trip settings of the CREFS fan motors, in combination with an apparent inadequate methodology for determining breaker TOL settings and failure to test the breaker TOL settings, was a performance deficiency that resulted in loss of functionality of the single train CREFS and warranted a significance evaluation.
The inspectors concluded that the finding is greater than minor in accordance with IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue Screening, November 2, 2006, because the finding is associated with the containment barrier cornerstone of reactor safety. The inspectors evaluated the finding using IMC 0609, Appendix A, Determining the Significance of Reactor Inspection Findings for At-Power Situations. The finding screens as (Green) very low safety significance, as it only represents a degradation of the radiological barrier function provided for the control room. The loss of CREFS fans during a release could result in increased dose to the operator in the control room potentially affecting control room habitability. Although the finding involved a potential failure of CREFS to provide its filtration function, the simultaneous occurrence of low outside temperature, degraded grid voltage and a radiological release is of very low probability. The finding for the failure to provide the correct thermal overload trip settings is a design deficiency that has a cross-cutting aspect in the area of human performance in that resources were not effective in maintaining long-term plant safety by maintenance of design margins.
Enforcement:
10 CFR, Part 50, Appendix B, Criterion III, Design Control, requires that the design bases are correctly translated into specifications, drawings, procedures and instructions. Contrary to these requirements, the licensee did not establish the correct thermal overload trip settings for the CREFS fan motors for MR 05-016, VNCR Emergency Fan Motor Modification, resulting in a failure to maintain sufficient design margin from the maximum expected running current to the thermal overload trip setting.
As a result, CREFS Fan W-14 B tripped on thermal overload during testing with low outside ambient air temperature (approximately -11 EF) and it has been shown by analysis that a trip of fan W-14A would also have been likely for the combination of low temperature and degraded grid voltage. Because this violation is of very low safety significance and has been entered into the licensees corrective action program (AR0107542), this violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy (NCV 05000266/2007002-02; 0500301/2007002-02).
The licensee issued an engineering change, ECN 1601, to revise the trip setpoint to a range of 11.5 to 12.3 amps and both fans subsequently passed post maintenance and surveillance testing, restoring system operability. The licensee performed Root Cause Analysis RCE 01075472-01, Root Cause Analysis of Control Room Emergency Filter Fan System (CREFS) Motor Tripping, for these issues. The licensees planned corrective actions included the creation and implementation of a Design Guide for engineers to select new motor overload relays consistent with the National Electric Code to ensure that the design and licensing bases and the motor protection requirements were appropriately considered for modifications. The licensee also planned corrective actions to generically ensure that the initial installation testing requirements for breaker TOL trip settings are established and verified periodically. Additionally, planned corrective actions to change maintenance procedures will provide methods for setting and testing motor overload relays, consistent with the issued Design Guide.
.2 Licensee Response to Increased Frequency of Draining of the Unit 2 B Steam
Generator Vent Line
a. Inspection Scope
On November 14, 2006, the Unit 2 polar crane main hook contacted the B Steam Generator vent line, as discussed in Section 40A3 of NRC Inspection Report 05000266/2006013; 05000301/2006013. The licensee concluded the line was operable but degraded, isolated the line with the first-off valve, 2MS-212. The licensee also implemented compensatory measures, which included periodic ultrasonic testing (UT) measurements of water level in the vent line and subsequent draining of that line, as required. Valve 2MS-212 started leaking which admitted steam/condensate into the pipe. The vent line piping downstream of the valve was to be maintained less than full to address a potential Generic Letter 96-06 overpressure concern, with 2MS-212 closed, a valve which was normally open during power operations. To maintain the line less than full, more frequent UT of the piping outside containment was required, as well as more frequent draining of the piping. In February 2007, the inspectors evaluated the stations Operational Decision-Making Issue Evaluation Document (ODMI) that addressed options to obviate the need for the frequent UT and draining of the line.
The inspectors observed performance of the UT measurements, attended the licensees working meeting to discuss the ODMI and reviewed related documentation. The inspectors concluded the licensees evaluation of options and subsequent decision to reposition the first-off isolation valve, 2MS-212, to the normal open configuration (so the entire length of the line was open back to the Steam Generator) was consistent with the station approved ODMI process and appropriate for the identified issues. Finally, the inspectors observed portions of the operations evolutions associated with the re-opening of the 2MS-212 valve. The review by the inspectors constituted one inspection procedure sample.
b. Findings
No findings of significance were identified.
4OA6 Meetings
.1 Exit Meeting
On April 3, 2007, the resident inspectors presented the inspection results to Mr. D. Koehl and members of his staff, who acknowledged the findings. The licensee did not identify any information, provided to or reviewed by the inspectors, as proprietary.
.2 Interim Exit
Interim exits were conducted for:
- Biennial Operator Requalification Program Inspection with Mr. R. Amundson, General Supervisor Operations Training, Point Beach Nuclear Plant on January 17, 2007; and
- The (Open) Unresolved Item (URI 05000266/2004010-01; 05000301/2004010-01)
Operational Implementation of Alternate Shutdown Capability on January 17, 2007.
ATTACHMENT:
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee Personnel
- R. Amundson, General Supervisor Operations Training
- C. Butcher, Site Engineering Director
- G. Casadonte, Fire Protection Coordinator
- G. Corell, Radiation Protection General Supervisor
- F. Flentje, Licensing Supervisor
- T. Gemskie, Emergency Preparedness Supervisor
- R. Harrsch, Operations Manager
- J. Schleif, Assistant Operations Manager
- C. Jilek, Maintenance Rule Coordinator
- R. Johnson, Senior Emergency Preparedness Coordinator
- T. Kendall, Engineering Senior Technical Advisor
- D. Koehl, Site Vice-President
- G. LeClair, Radiation Protection Supervisor
- J. McCarthy, Director of Site Operations
- J. McNamara, Engineering Supervisor
- C. Monarch, Fire Protection Engineer
- R. Mrozinsky, Appendix R Engineer
- P. Nicholson, Fire Protection Engineer
- G. Packard, Plant Manager
- L. Peterson, Design Engineer Manager
- M. Ray, Regulatory Affairs Manager
- D. Schuelke, Radiation Protection and Chemistry Manager
- L. Schofield, Employee Concerns Program Manager
- J. Schweitzer, Manager of Projects
- G. Sherwood, Engineering Programs Manager
- C. Sizemore, Training Manager
- B. Vandervelde, Maintenance Manager
- S. Tulley, Emergency Preparedness Manager
- P. Wild, Design Engineering Projects Supervisor
Nuclear Regulatory Commission
- P. Louden, Chief, Reactor Projects, Branch 5
Attachment
ITEMS OPENED, CLOSED, AND DISCUSSED
Opened and Closed
- 05000301/2007002-01 NCV Failure to Take Corrective Actions for Cold Weather Issues Prior to the Onset of Cold Weather (Section 1R01)
- 05000266/2007002-02; NCV Failure to Maintain Design Margin for Control Room
- 05000301/2007002-02 Emergency Filtration Fan Thermal Overload Trips (Section 4OA3.1)
Discussed
- 05000266/2004010-01; URI Operational Implementation of Alternate Shutdown
- 05000301/2004010-01 Capability (Section 1R05.2)
Attachment