IR 05000266/2021002

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Integrated Inspection Report 05000266/2021002, 05000301/2021002, and 07200005/2021001
ML21208A420
Person / Time
Site: Point Beach  NextEra Energy icon.png
Issue date: 07/29/2021
From: Nestor Feliz-Adorno
Reactor Projects Region 3 Branch 4
To: Strope M
Point Beach
References
IR 2021001, IR 2021002
Download: ML21208A420 (31)


Text

SUBJECT:

POINT BEACH NUCLEAR PLANT - INTEGRATED INSPECTION REPORT 05000266/2021002, 05000301/2021002, AND 07200005/2021001

Dear Mr. Strope:

On June 30, 2021, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Point Beach Nuclear Plant. On July 12, 2021, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

Two findings of very low safety significance (Green) are documented in this report. Two of these findings involved violations of NRC requirements. We are treating these violations as non-cited violations (NCVs), consistent with Section 2.3.2 of the Enforcement Policy.

A licensee-identified violation, which was determined to be of very low safety significance, is documented in this report. We are treating this violation as a non-cited violation (NCV)

consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violations, or the significance or severity of the violations documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001, with copies to the Regional Administrator, Region III; the Director, Office of Enforcement; and the NRC Resident Inspector at Point Beach Nuclear Plant.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with copies to the Regional Administrator, Region III, and the NRC Resident Inspector at Point Beach Nuclear Plant.

July 29, 2021 This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room, in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Néstor J. Féliz Adorno, Chief Branch 4 Division of Reactor Projects Docket Nos. 05000266; 05000301; and 07200005 License Nos. DPR-24, DPR-27

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000266, 05000301, 07200005

License Numbers:

DPR-24 and DPR-27

Report Numbers:

05000266/2021002,05000301/2021002, 07200005/2021001

Enterprise Identifier:

I-2021-002-0098 and I-2021-001-0159

Licensee:

Nextera Energy Point Beach, LLC

Facility:

Point Beach Nuclear Plant

Location:

Two Rivers, WI

Inspection Dates:

March 01, 2021 to June 30, 2021

Inspectors:

J. Cassidy, Senior Health Physicist

J. Dalzell, Reactor Inspector

R. Edwards, Senior Health Physicist

T. Hartman, Senior Resident Inspector

V. Petrella, Resident Inspector

R. Ruiz, Project Engineer

Approved By:

Néstor J. Féliz Adorno, Chief

Branch 4

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Point Beach Nuclear Plant, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. A licensee-identified non-cited violation is documented in report section: 7115

List of Findings and Violations

SCBA Regulator Testing and Maintenance Cornerstone Significance Cross-Cutting Aspect Report Section Occupational Radiation Safety Green NCV 05000266,05000301/2021002-01 Open/Closed

[H.3] - Change Management 71124.03 The inspectors identified a Green finding and associated Non-cited Violation (NCV) of 10 CFR 20.1703(c)(4)(vii) for the licensee failure to maintain a respiratory protection program that includes written procedures regarding storage, issuance, maintenance, repair, testing, and quality assurance of respiratory protection equipment. Although the licensees procedure indicated that the testing schedule was consistent with the vendors manual, the procedural required testing periodicity was twice that specified by the vendor. Consequently, the licensees procedure failed to ensure the maintenance and testing of components used in situations with highest radiological risk and that could also be used in atmospheres that are Immediately Dangerous to Life and Health.

Breathing Air Quality Testing and Analysis Cornerstone Significance Cross-Cutting Aspect Report Section Occupational Radiation Safety Green NCV 05000266,05000301/2021002-02 Open/Closed

[H.13] -

Consistent Process 71124.03 The inspectors identified a Green finding and associated Non-cited Violation (NCV) of 10 CFR 20.1703(c)(4)(v) when the licensee failed to implement written procedures regarding breathing air quality as part of the respiratory protection program. Specifically, licensee procedures required Air Quality Testing be performed quarterly (per OSHA 1910.134 and NRC Regulatory Guide 8.15); however, the licensee performed the testing at an annual frequency. Consequently, the reduced frequency challenged the licensees ability to provide adequate protection to the workers wearing self-contained breathing apparatuses.

Additional Tracking Items

None.

PLANT STATUS

Unit 1 began the inspection period at rated thermal power. On April 20, 2021, reactor power was reduced to approximately 55 percent for turbine stop valve testing and condenser waterbox cleaning. On April 21, 2021, the unit was returned to rated thermal power, and remained at or near full power throughout the remainder of the inspection period.

Unit 2 began the inspection period at rated thermal power and remained at or near full power throughout the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved Ips, with their attached revision histories, are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met, consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

Starting on March 20, 2020, in response to the National Emergency declared by the President of the United States on the public health risks of the coronavirus (COVID-19), resident and regional inspectors were directed to begin telework and to remotely access licensee information using available technology. During this time, the resident inspectors performed periodic site visits each week, increasing the amount of time on site as local COVID-19 conditions permitted.

As part of their onsite activities, resident inspectors conducted plant status activities as described in IMC 2515, Appendix D; observed risk significant activities; and completed on site portions of IPs. In addition, resident and regional baseline inspections were evaluated to determine if all, or a portion, of the objectives and requirements stated in the IP could be performed remotely. If the inspections could be performed remotely, they were conducted per the applicable IP. In some cases, portions of an IP were completed remotely and on site. The inspections documented below met the objectives and requirements for completion of the IP.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Seasonal Extreme Weather Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated readiness for seasonal extreme weather conditions prior to the onset of extreme high temperatures on June 3, 2021.

External Flooding Sample (IP Section 03.03) (1 Sample)

(1) The inspectors evaluated flood protection barriers, mitigation plans, procedures, and equipment for consistency with the licensees design requirements and risk analysis assumptions for coping with external flooding on June 24, 2021.

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Unit 1 train B containment spray system on May 27, 2021
(2) Unit 1 motor-driven auxiliary feedwater pump on May 27, 2021
(3) Unit 1 train A safety injection system on June 29, 2021

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:

(1)fire zones 304N, 304S, and 305 on April 6, 2021 (2)fire zones 162, 163, 164, 165, and 166 on April 23, 2021 (3)fire zone 238 on April 23, 2021 (4)fire zone 237 on April 23, 2021 (5)fire zone 240 on April 23, 2021

Fire Brigade Drill Performance Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated the onsite fire brigade training and performance during an unannounced fire drill on May 29, 2021.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the main control room during safety injection system testing on April 8, 2021, and during the Unit 1 down power from 100 percent power to 55 percent power on April 20, 2021.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated a licensed operator simulator exam on May 24, 2021.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (2 Samples)

The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended function:

(1)leading edge flow meter inputs to reactor thermal output indication: failures on February 7, February 28, March 9, March 19, March 21, and March 28, 2021

(2) G-05 gas turbine exceeds reliability performance criteria

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1)elevated risk for the Unit 1 train B safeguards logic testing on April 15, 2021 (2)elevated risk for the Unit 1 train B reactor protection logic testing on April 15, 2021 (3)elevated risk for the Unit 2 blue inverter (2DY-02) maintenance and inspection on May 3, 2021 (4)last minute rescheduling of maintenance activities due to conservative grid operations on June 28-29, 2021

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (5 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:

(1)pipe hanger found moved on Unit 1 component cooling water system (2)elevated temperature on Unit 2 turbine-driven auxiliary feedwater pump inboard packing gland

(3) Prompt Operability Determination, 2386499-01, CCW Piping Analysis Not Updated for Removed Pipe Penetration
(4) ASME Code Case N-513-4 evaluation of pin hole leak in the 6" CCW piping adjacent to valve 2CC-753.

(5)increased frequency of adding nitrogen to the power-operated relief valve accumulator

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the following post-maintenance test activities to verify system operability and functionality:

(1)0-SOP-IA-006, K-2B Instrument Air Compressor Recovery from Maintenance, after maintenance on K-002B Instrument Air Compressor on April 9, 2021

(2) PC 29, Gas Turbine and Auxiliary Diesel Load Test, after maintenance on G-05 Emergency Diesel Generator on April 5, 2021 (3)1RMP 9056-2, Calibration and Testing of Safety Related Protective Relays A-06 after replacement of 1-62-1/A-06 and 1-62-2/A-06 relays on April 29, 2021 (4)2RMP 9036-6, 2DY-02 Blue Channel Instrument Bus Static Inverter Maintenance Procedure after maintenance on the 2DY-02 Blue Channel Instrument Bus Static Inverter on May 4, 2021

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Surveillance Tests (other) (IP Section 03.01)

(1) IT 45 Train B, Safety Injection Valves Train B Unit 2, on April 8, 2021
(2) TS 81, Emergency Diesel Generator G-01 Monthly, on April 18, 2021
(3) IT 08A, Cold Start of Turbine-Driven Auxiliary Feed Pump and Valve Test (Quarterly)

Unit 1, on April 19, 2021

(4) TS 83, Emergency Diesel Generator G-03 Monthly, on June 2, 2021

Inservice Testing (IP Section 03.01) (1 Sample)

(1) IT 07D/E/F, P-32D/E/F Service Water Pumps Comprehensive Test, on May 12, 2021

FLEX Testing (IP Section 03.02) (1 Sample)

(1)0-SOP-FLEX-003, Flex Portable Diesel Low Pressure Pump Operation Z-2003A & Z-2003B, on June 2, 2021

71114.06 - Drill Evaluation

Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01) (1 Sample)

(1) A full-scale emergency preparedness site drill conducted on April 28,

RADIATION SAFETY

71124.02 - Occupational ALARA Planning and Controls

Radiological Work Planning (IP Section 03.01) (4 Samples)

The inspectors evaluated the licensees radiological work planning for the following work activities.

(1) Remove/Reinstall Reactor Vessel (RV) Head under Radiation Work Permit (RWP)20-1016
(2) Reactor Coolant System (RCS) Leak Repair under Radiation Work Permit (RWP)20-1062
(3) Scaffolding Containment Outage Activities under Radiation Work Permit (RWP)20-1025
(4) Scaffolding Containment Outage Activities under Radiation Work Permit (RWP)20-2025 Verification of Dose Estimates and Exposure Tracking Systems (IP Section 03.02) (4 Samples)

The inspectors evaluated dose estimates and exposure tracking for the following work activities.

(1) Remove/Reinstall RV Head under Radiation Work Permit (RWP) 20-1016
(2) RCS Leak Repair under Radiation Work Permit (RWP) 20-1062
(3) Scaffolding Containment Outage Activities under Radiation Work Permit (RWP)20-1025
(4) Scaffolding Containment Outage Activities under Radiation Work Permit (RWP)20-2025

71124.03 - In-Plant Airborne Radioactivity Control and Mitigation

Permanent Ventilation Systems (IP Section 03.01) (1 Sample)

The inspectors evaluated the configuration of the following permanently installed ventilation systems:

(1) Control Room Ventilation System - Common Unit

Self-Contained Breathing Apparatus for Emergency Use (IP Section 03.04) (1 Sample)

(1) The inspectors evaluated the licensees use and maintenance of self-contained breathing apparatuses.

71124.04 - Occupational Dose Assessment

Source Term Characterization (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated licensee performance as it pertains to radioactive source term characterization.

External Dosimetry (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated licensee performance as it pertains to external dosimetry that is used to assign occupational dose.

Internal Dosimetry (IP Section 03.03) (1 Sample)

The inspectors evaluated the internal dosimetry program implementation.

(1) The inspectors reviewed the Whole Body Counts associated with a contamination event on October 9, 2020.

Special Dosimetric Situations (IP Section 03.04) (1 Sample)

The inspectors evaluated the following special dosimetric situation:

(1) Licensees implementation of requirements to manage radiation protection of shallow dose equivalent for AR 02330629.

71124.05 - Radiation Monitoring Instrumentation

Walkdowns and Observations (IP Section 03.01) (8 Samples)

The inspectors evaluated the following radiation detection instrumentation during plant walkdowns:

(1) GM Tube-Based Ratemeter and Area Monitor - MGP AMP-200 7717-004 ready for use
(2) GM Tube-Based Ratemeter and Area Monitor - MGP AMP-100 479291 ready for use
(3) Ion Chamber Survey Meter - Ludlum 9-3 330694 ready for use
(4) Ion Chamber Survey Meter - Eberline RO20 472966 330694 ready for use
(5) Extendable Survey Meter - Mirion Telepole 330482 ready for issue
(6) Personnel Contamination Monitor - ARGOS 0712-047 at auxiliary building exit
(7) Tool and Equipment Monitor - Mirion Cronos-4 1511-198 at auxiliary building exit
(8) Portal Monitor - Mirion GEM-5 0712-118 at auxiliary building exit

71124.07 - Radiological Environmental Monitoring Program

Environmental Monitoring Equipment and Sampling (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated environmental monitoring equipment and observed collection of environmental samples.

Radiological Environmental Monitoring Program (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated the implementation of the licensees radiological environmental monitoring program.

GPI Implementation (IP Section 03.03) (1 Sample)

(1) The inspectors evaluated the licensees implementation of the Groundwater Protection Initiative program to identify incomplete or discontinued program elements.

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification The inspectors verified licensee performance indicators submittals listed below:

MS05: Safety System Functional Failures (SSFFs) Sample (IP Section 03.04)===

(1) Unit 1 (May 1, 2020 through April 30, 2021)
(2) Unit 2 (May 1, 2020 through April 30, 2021)

BI02: RCS Leak Rate Sample (IP Section 03.11) (2 Samples)

(1) Unit 1 (May 1, 2020 through April 30, 2021)
(2) Unit 2 (May 1, 2020 through April 30, 2021)

71152 - Problem Identification and Resolution

Annual Follow-up of Selected Issues (IP Section 02.03) (1 Sample)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) National Fire Protection Association Standard (NFPA) 805 fire protection program implementation deficiencies

OTHER ACTIVITIES

- TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL 60854 - Preoperational Testing of an ISFSI The inspectors reviewed documents, interviewed plant personnel, and performed in-field observations to assess the licensees preoperational testing of an ISFSI. The inspectors performed an independent assessment that the licensee had adequately demonstrated its readiness to safely perform ISFSI loading and unloading operations. Specifically, the inspectors evaluated the following:

(1) The licensee performed preoperational dry run activities. The inspectors evaluated following activities:

The inspectors observed welding dry run activities on April 12-14, 2021. Specifically, the inspectors observed closure welding of a canister and non-destructive examination of the welds.

The inspectors observed processing dry run activities on April 26-28, 2021. Specifically, the inspectors observed canister reflood evolution, bulk water removal and blowdown, vacuum drying operations, and helium backfill.

The inspectors observed MPC insertion and HI-STORM transport dry run activities on May 10-12, 2021. Specifically, the inspectors observed insertion and removal of a MPC into a HI-STORM FW, transport of HI-STORM FW to the ISFSI Pad and placement of the cask on the ISFSI Pad.

The inspectors observed fuel loading dry run activities on May 24-17, 2021. Specifically, the inspector observed movement of the HI-TRAC between the decontamination pit and the spent fuel pool, fuel moves, and MPC lid placement and removal.

(2) Fuel Selection

The inspectors reviewed cask fuel selection packages to verify that the licensee was loading fuel in accordance with TS 2.1, Fuel to be Stored in the HI-STORM FW MPC Storage System.

60855 - Operation of an ISFSI The inspectors evaluated the licensees independent spent fuel storage installation cask loadings on June 1-5, 2021. Specifically, the inspectors observed the following activities:

movement of the HI-TRAC from the decontamination pit to the spent fuel pool

spent fuel loading and verification activities

placement of the damaged fuel canister lids and MPC lid

movement of the HI-TRAC from the spent fuel pool to the decontamination pit

canister welding and non-destructive weld evaluations

drying evolutions

transfer of the MPC from the HI-TRAC to the HI-STORM FW The inspectors performed walkdowns of the ISFSI pad, including independent radiation surveys, and walkdowns of the ISFSI haul path and vertical cask transporter (VCT).

The inspectors evaluated the following:

selected corrective action program action requests

selected 72.48 screenings and evaluations 60856 - Review of 10 CFR 72.212(b) Evaluations The inspectors evaluated the licensees compliance with the requirements of 10 CFR 72.212 and 10 CFR 72.48, as well the licensees revised engineering documentation and calculations associated with the HI-STORM FW CoC 072-1032, Revision 6. Prior to use of a dry cask storage system, the licensee is required to perform written evaluations in accordance with 10 CFR 72.212(b)(5)(i) to establish that the terms, conditions, and specifications of a CoC or an amended CoC have been met. Specifically, the inspectors performed an in-office review of the following from March 1-May 30, 2021:

10 CFR 72.212 Evaluation Report for the HI-STORM FW CoC 072-1032, Revision 6 and associated calculations

EC 294818, HI-STORM FW Cask System Licensing and Operation and supporting engineering changes and referenced calculations

HI-TRAC Lifting Yoke Assembly

Vertical Cask Transporter Seismic Stability Analysis

Auxiliary Building and Crane Structural Analysis

Stack-up and MPC Transfer Seismic Analysis

ISFSI Pad Structural Capacity Qualification

INSPECTION RESULTS

SCBA Regulator Testing and Maintenance Cornerstone Significance Cross-Cutting Aspect Report Section Occupational Radiation Safety Green NCV 05000266,05000301/2021002-01 Open/Closed

[H.3] - Change Management 71124.03 The inspectors identified a Green finding and associated Non-cited Violation (NCV) of 10 CFR 20.1703(c)(4)(vii) for the licensee failure to maintain a respiratory protection program that includes written procedures regarding storage, issuance, maintenance, repair, testing, and quality assurance of respiratory protection equipment. Although the licensees procedure indicated that the testing schedule was consistent with the vendors manual, the procedural required testing periodicity was twice that specified by the vendor. Consequently, the licensees procedure failed to ensure the maintenance and testing of components used in situations with highest radiological risk and that could also be used in atmospheres that are Immediately Dangerous to Life and Health.

Description:

The licensee replaced the Self-Contained Breathing Apparatus (SCBA) units at the site with the SCOTT Air-Pak X3 Model 4.5 in October 2019 to limit intake of radioactive material. The licensee reviewed/revised procedure NP 4.2.32 Respiratory Protection Program to support the equipment change.

The inspectors identified that the procedure contained a testing frequency that was inconsistent with the frequency provided by the vendor. The current revision of procedure NP 4.2.32 Respiratory Protection Program (Revision 21) Attachment A SCBA Equipment Information indicates that Functional Flow Testing will be performed every two years (per SCOTT Air-Pak X3 Model 4.5 Operating and Maintenance Instructions) <emphasis added>.

However, the inspectors reviewed the Operating & Maintenance for the SCOTT Air-Pak X3 Pro & Air-Pak X3 Snap-Change Model 2.2/4.5/5.5 Rev F 2/18 and found "Periodic Testing - SCOTT recommends that this respirator be inspected and tested by a SCOTT Authorized Service Center using SCOTT Authorized Test Equipment at least once a year

<emphasis added>. Heavy use and/or severe service conditions may require more frequent inspection and testing. This recommendation is in addition to all other cleaning and maintenance procedures."

The licensee did not have an evaluation or technical basis on this issue and could not demonstrate that extending the frequency of required maintenance and testing did not degrade performance of components used in situations with highest radiological risk and could also be used in atmospheres that are Immediately Dangerous to Life and Health.

Consequently, all of the units missed the testing maintenance that should have been performed in October 2020 had the units been tested at the frequency of at least once a year.

Corrective Actions: The licensee rescheduled the vendor maintenance of the SCBA regulators to June 15 to 17, 2021. Additionally, Radiation Protection and the Fire Protection Coordinator were evaluating the issue to determine actions needed.

Corrective Action References: AR02391216

Performance Assessment:

Performance Deficiency: The licensee failed to maintain written procedures regarding maintenance, repair, testing, of respiratory protection equipment as required by 10 CFR 20.1703(c)(4)(vii). Although the licensees procedure (NP 4.2.32 Respiratory Protection Program) indicated that the testing schedule was consistent with the vendors manual, the procedural required testing periodicity was twice that specified by the vendor.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Plant Facilities/Equipment and Instrumentation attribute of the Occupational Radiation Safety cornerstone and adversely affected the cornerstone objective to ensure the adequate protection of the worker health and safety from exposure to radiation from radioactive material during routine civilian nuclear reactor operation.

Specifically, licensee procedures were not revised to incorporate the vendor testing instructions (required by the procedure) when new SCBAs were implemented by the licensee.

Additionally, the licensee did not perform an evaluation of the extended periodicity to demonstrate it would not result in an actual personnel safety concern.

Significance: The inspectors assessed the significance of the finding using Appendix C, Occupational Radiation Safety SDP. The inspectors assessed the significance of the finding using Appendix C, Occupational Radiation Safety SDP. The inspectors determined that the finding was of very low safety significance (i.e., Green) because:

(1) it did not involve as-low-as reasonably achievable planning or work controls,
(2) there was no overexposure,
(3) there was no substantial potential for an overexposure, and
(4) the ability to assess dose was not compromised.

Cross-Cutting Aspect: H.3 - Change Management: Leaders use a systematic process for evaluating and implementing change so that nuclear safety remains the overriding priority.

Specifically, the process used to implement the new SCBAs did not update the maintenance and testing procedure with the vendors instructions for the new SCBAs.

Enforcement:

Violation: 10 CFR 20.1703(c)(4)(vii) states The licensee shall implement and maintain a respiratory protection program that includes written procedures regarding storage, issuance, maintenance, repair, testing, and quality assurance of respiratory protection equipment.

Procedure NP 4.2.32 Respiratory Protection Program, Revision 21, Attachment A SCBA Equipment Information states functional flow testing will be performed every two years (per SCOTT Air-Pak X3 Model 4.5 Operating and Maintenance Instructions).

SCOTT Air-Pak X3 Model 4.5 Operating and Maintenance Instructions (Rev F 2/18)states Periodic Testing - SCOTT recommends that this respirator be inspected and tested (including functional flow testing) by a SCOTT Authorized Service Center using SCOTT Authorized Test Equipment at least once a year.

Contrary to the above, as of October 2019, the licensee failed to maintain a respiratory protection program that includes written procedures regarding storage, issuance, maintenance, repair, testing, and quality assurance of respiratory protection equipment.

Specifically, procedure NP 4.2.32, Attachment A specifies functional flow testing for its SCBAs every two years and per the vendors instructions; however, the vendors instructions specify the testing at least once per year.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Breathing Air Quality Testing and Analysis Cornerstone Significance Cross-Cutting Aspect Report Section Occupational Radiation Safety Green NCV 05000266,05000301/2021002-02 Open/Closed

[H.13] -

Consistent Process 71124.03 The inspectors identified a Green finding and associated Non-cited Violation (NCV) of 10 CFR 20.1703(c)(4)(v) when the licensee failed to implement written procedures regarding breathing air quality as part of the respiratory protection program. Specifically, licensee procedures required Air Quality Testing be performed quarterly (per OSHA 1910.134 and NRC Regulatory Guide 8.15); however, the licensee performed the testing at an annual frequency. Consequently, the reduced frequency challenged the licensees ability to provide adequate protection to the workers wearing self-contained breathing apparatuses.

Description:

Procedure NP 4.2.32 Respiratory Protection Program Revision 21 Attachment A SCBA Equipment Information requires Air Quality Testing will be performed quarterly (per OSHA 1910.134 and NRC Regulatory Guide 8.15). Additionally, the licensee developed a Technical Basis Document, HP-100-013020 SCBA Air Quality Requirements dated February 2, 2020.

This assessment was performed in support of the decision to contract the filling of SCBA cylinders to an offsite vendor and abandon the equipment used to perform onsite filling of SCBA cylinders. The assessment concluded that Point Beach Nuclear Plant shall request the offsite vendor to provide air quality test records a minimum of four times per year.

The licensee started using a contracted vendor to refill SCBA cylinders in May 2019. The records of breathing air quality analysis provided by licensee indicated that the testing and analysis was only performed once per year. Additionally, this testing was performed in February or March when the relative humidity is lower than other times of the year.

Consequently, the results for the required dew point measurement of the compressed air may not be representative for the entire year.

Corrective Actions: Radiation Protection and the Fire Protection Coordinator were evaluating the issue to determine actions needed.

Corrective Action References: AR02391216

Performance Assessment:

Performance Deficiency: The licensee failed to implement written procedures for the frequency of testing breathing air quality as required by 10 CFR 20.1703(c)(4)(v). Although A of Licensee procedure NP 4.2.32 Respiratory Protection Program required Air Quality Testing be performed quarterly (per OSHA 1910.134 and NRC Regulatory Guide 8.15), the inspectors identified that the licensee was performing the testing on an annual frequency.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Plant Facilities/Equipment and Instrumentation attribute of the Occupational Radiation Safety cornerstone and adversely affected the cornerstone objective to ensure the adequate protection of the worker health and safety from exposure to radiation from radioactive material during routine civilian nuclear reactor operation.

Specifically, the licensee determined that breathing air quality must be tested and analyzed on a quarterly basis to maintain certification but did not implement this requirement when a vendor was selected to refill the SCBA bottles. The reduced frequency challenged the licensees ability to provide adequate protection to the workers wearing self-contained breathing apparatuses.

Significance: The inspectors assessed the significance of the finding using Appendix C, Occupational Radiation Safety SDP. The inspectors determined that the finding was of very low safety significance (i.e., Green) because:

(1) it did not involve as-low-as reasonably achievable planning or work controls,
(2) there was no overexposure,
(3) there was no substantial potential for an overexposure, and
(4) the ability to assess dose was not compromised.

Cross-Cutting Aspect: H.13 - Consistent Process: Individuals use a consistent, systematic approach to make decisions. Risk insights are incorporated as appropriate. Specifically, the process used to have an off-site vendor to fill SCBA bottles did not systematically implement the results from the licensee developed Technical Basis Document, HP-100-013020 SCBA Air Quality Requirements

Enforcement:

Violation: 10 CFR 20.1703(c)(4)(v) states The licensee shall implement and maintain a respiratory protection program that includes written procedures regarding breathing air quality.

Licensee procedure NP 4.2.32 Respiratory Protection Program Revision 21, in part, implements the respiratory protection program. Attachment A SCBA Equipment Information of this procedure required Air Quality Testing be performed quarterly (per OSHA 1910.134 and NRC Regulatory Guide 8.15).

Contrary to the above, since May 2019, the licensee failed to implement a respiratory protection program that includes written procedures regarding breathing air quality.

Specifically, the licensee failed to implement procedure NP 4.2.32 requirements for quarterly testing of air quality for air used in SCBAs. The licensee had only performed the testing in February 20, 2019, March 2020, and February 2021.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Licensee-Identified Non-Cited Violation 71152 This violation of very low safety significance was identified by the licensee and has been entered into the licensee corrective action program and is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Violation: Point Beach License Condition 4.F requires, in part, that the licensee implement and maintain in effect all provisions of the approved Fire Protection Program that complies with 10 CFR 50.48(a) and 10 CFR 50.48(c), NFPA [National Fire Protection Association]

Standard NFPA 805, as approved in the Safety Evaluation Report (SER) dated September 8, 2016. Section 2.4.3.3 of NFPA 805 states, in part, that the PSA [Probabilistic Safety Assessment] approach, methods, and data shall be appropriate for the nature and scope of the change being evaluated, be based on the as-built and as-operated and maintained plant, and reflect the operating experience at the plant.

Contrary to the above, from February 14, 2017, to May 23, 2020, the licensee failed to implement and maintain in effect all provisions of the approved Fire Protection Program that complies with 10 CFR 50.48(a) and 10 CFR 50.48(c) because the PSA approach, methods, and data were not based on the as-built and as-operated and maintained plant. Specifically, the supporting calculations for the fire PSA were not based on the as-built service water system because they did not account for the potential of spurious operation of service water valves. As a result, the licensee did not account for the potential spurious valve operation impact on service water flow during NFPA 805 fire events.

Significance/Severity: Green. The inspectors screened this finding in accordance with Inspection Manual Chapter (IMC) 0609, Significance Determination Process, Attachment 4, Initial Characterization of Findings. The finding was associated Fire Protection and affected the ability to reach and maintain safe shutdown conditions in the event of a fire and was therefore reviewed using IMC 0609, Appendix F, Attachment 1, Fire Protection Significance Determination Process Worksheet. The finding was screened as a finding of very low safety significance (Green) in accordance with Step 1.4.7, Post-fire Safe Shutdown, Question 1.4.7-C which asked, Does the fire finding adversely affect the ability to reach and maintain hot shutdown/hot standby or safe and stable condition using the credited safe shutdown success path? The licensee revised calculations and determined that post-fire safe shutdown was not affected because the service water system would remain operational with two service water pumps following spurious operation of four valves.

Corrective Action References: AR 02331854 Observation: Review of Selected Fire Protection Issues 71152 Since the plant's transition to 10 CFR 50.48(c) [National Fire Protection Association (NFPA)

Standard 805] in February 2017, the licensee has identified a number of issues associated with the fire protection program. The inspectors selected three of these issues and performed an in-depth review of the associated Action Requests (ARs) and corrective actions to ensure that the licensee implemented corrective actions commensurate with the significance of the identified issues.

AR 02286581, "NFPA 805 Documentation Incorrect" - The licensee identified incorrect statements in PRA [Probabilistic Risk Assessment] 8.1, Fire PRA Boundary Definition and Partitioning Notebook regarding fire compartment 122GRP. The licensee determined that multiple openings and non-fire rated doors existed in a barrier for which PRA 8.1 documented that Barrier wall and floor/ceiling segments qualify as fire rated construction and No unprotected combustible pathways to adjacent compartments existed. As part of the corrective actions and extent of condition the licensee performed walkdowns of other non-three hour rated barriers between fire compartments and identified numerous other discrepancies between PRA 8.1 and conditions in the field.

AR 02331840, "NFPA 805 Action Not Contained in Procedure" - The Nuclear Safety Capability Assessment (NSCA) credited closing blowdown isolation valves 1MS-5958 and 1MS-5959 by isolating instrument air using valves 1IA-3047 and 1IA-3048 in Fire Area A08 remotely from the control room. However, Emergency Operating Procedure EOP-2 directed operators to verify valves 1MS-5958 and 1MS-5959 were shut and, if not, to locally close them. As part of the corrective action to address this issue, the licensee revised NSCA Section 7.2.3.3 to credit EOP-2.

AR 02331854, "NFPA 805 Spurious Operation of Service Water Valves Not Considered" - The licensee identified that the NSCA and Fire PRA rely on the service water system to support several systems to ensure safe and stable shutdown. The licensee initially concluded that three (out of six) service water pumps would be required to support system operation. As a result of spurious operation of service water (SW) valves SW-2890, SW-2891, SW-2869, and SW-2870, there were several fire conditions where only two service water pumps would be available. The spurious operation of these valves was not considered in calculations 2012-006 and 2018-0016. The licensee reevaluated the operation of the service water system with only two SW pumps following the spurious operation of the identified valves and concluded that the SW system would deliver the required amount of water flow. The licensee subsequently revised calculations 2012-006 and 2018-0016 to demonstrate this.

The inspectors spoke with plant personnel regarding these three ARs in order to understand the issues, the appropriateness of the corrective actions, and the ultimate resolution. The inspectors reviewed the changes that were made to the relevant PRA documents, NSCA, and calculations, and performed walkdowns where necessary.

During the course of the review the inspectors concluded that the likely cause of these issues not being discovered and resolved during the transition to NFPA 805 was that the individuals and work groups involved in the transition to NFPA 805 did not effectively communicate and coordinate their activities. Based on the samples reviewed, once those concerns were identified, the licensee performed a detailed review of the NFPA 805 program and took corrective actions to disposition the issues. The inspectors reviewed a sample of these corrective actions, as documented above, and concluded that they were reasonable and appropriate. The inspectors determined that two of the issues evaluated by the licensee (AR 02286581 and AR 02331840) had associated minor violations that were identified by the licensee and were dispositioned in accordance with the NRC's policies. A License-Identified Violation related to AR 02331854 is documented in this report.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On July 12, 2021, the inspectors presented the integrated inspection results to Mr. M.

Strope, Site Vice President, and other members of the licensee staff.

On May 28, 2021, the inspectors presented the Independent Spent Fuel Storage Installation Pre-Operational Inspection results to Mr. M. Strope, Site Vice President, and other members of the licensee staff.

On June 10, 2021, the inspectors presented the Independent Spent Fuel Storage Installation Loading Inspection results to Mr. B. Woyak, Safety Assurance and Learning Site Director, and other members of the licensee staff.

On June 24, 2021, the inspectors presented the Radiation Protection inspection results to Mr. M. Holzmann, Operations Director, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

ALARA Plans

ALARA Package

No. R001

Dry Cask Storage ALARA Plan

VCT Load Testing Documentation Package

05/15/2014

HI-STORM FW Lift Bracket Documentation Package

03/10/2021

HI-TRAC VW Lift Yoke Documentation Package

03/30/2021

MPC FW Lift Cleat Assembly Documentation Package

03/01/2021

HI-TRAC VW Lift Yoke Load Test

09/30/2020

HI-TRAC VW Lift Yoke/Lift Lugs Load Test

2/04/2021

Certificate of Compliance No. 1032, Amendment No. 3

06/13/2011

Miscellaneous

HI-2200093

Loading Plan and Fuel Compatibility Report for Point Beach

and 4

GQP 9.6

Visual Examination of Welds

HPP-2951-300

MPC Sealing, Drying, and Backfilling

HPP-2951-500

8.5: HI-PORT Frequent Use Inspection Checklist

HPP-2951-600

MPC Unloading

MSLT-MPC-

Holtec

Helium Mass Spectrometer Leak Test Procedure

03/14/2018

NDE-401

Visible Dye Penetrant Examination Expanded Temperature

Applications

NP 8.4.7

Control of Safe Load Path and Rigging Manual

PBF-9240

Large Overhead Crane Daily Inspections

PR-AA-100-1003

Independent Spent Fuel Storage Installation / Dry Fuel

Storage Project Management

RDW 19.11

ISFSI Daily Surveillance

Procedures

RDW 19.12

ISFSI Thermal Surveillance

Self-Assessments RPT# PBN

19-005

Independent Spent Fuel Storage Installation

06/08/2019

60854

Work Orders

WO 40698177 04

PAB Crane Mechanical Inspection and Maintenance

01/08/2021

AR 02313689

ISFSI LIC DOC Site Disposition Gap

05/08/2019

AR 02313808

ISFSI Aging Management Program Ownership

05/09/2019

AR 02313880

AMP-Required ISFSI Related Inspection are Not On-Track

05/09/2019

60855

Corrective Action

Documents

AR 02315241

NA Finding: PBN ISFSI Station Ownership

05/22/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

AR 02322694

Repairs for 2017 VSC Annual Inspection

07/29/2019

AR 02322696

Repairs for 2018 Annual VSC Inspection

07/29/2019

AR 02324212

Repairs for 2019 Annual VSC Inspection

08/12/2019

AR 02369116

ISFSI MPC Minimum Wall Thickness Verification

09/23/2020

AR 02394406

Dry Run Work Delay Observation

05/27/2021

AR 02394673

PAB Crane Locked Up While Performing HPP-2951-200

06/01/2021

AR 02394766

FM On Top of DD45 Discovered During Cask Map

06/02/2021

AR 02395083

HPP-29510-300 MPC Sealing, Drying and Backfilling

06/04/2021

AR 02395522

Air Sample Greater Than Expected from the Vacuum Drying

Skid

06/10/2021

CFR 50.59

Screen

20-0067

EC 291715: Z-17 SFP Crane Upgrades

Engineering

Changes

CFR 72.48

Screen

2019-0091

VSC-INSP-05 Lead Cask Inspection

08/15/2019

CFR 72.212 Evaluation Report for HI-SOTRM FW

Inspection of Rigging Components

03/31/2021

CFR 72.48

Screen NUH-

AMP-01

NUHOMS Aging Management Program

06/27/2019

CFR 72.48

Screen NUH-

INSP-06

High Burnup Fuel Aging Management Plan

06/27/2019

Miscellaneous

NPM 2017-0106

Demonstration of NDE-401, "Visible Dye Penetrant

Examination Expanded Temperature Applications"

09/15/2017

MSLT-MPC-

Holtec

Helium Leak Test Report for Multipurpose Canister

06/05/2021

NDE Reports

Report No.

917882-200

Liquid Penetrant Examination Results - Lid to Shell Weld

06/03/2021

Radiological Surveys Performed at ISFSI Used to

Demonstrate Compliance with 10 CFR 72.104

05/03/2021

Periodic Radiological Surveys Performed at the ISFSI

05/03/2021

Radiation

Surveys

Survey PBPROD-

MPC 200 HI-STORM CoC Survey

06/05/2021

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

M-20210606-6

Survey PBPROD-

M-20210607-5

MPC 200 HI-STORM Loaded for Transport

06/07/2021

Survey PBPROD-

M-20210609-9

MPC 200 ISFSI Pad Boundary Survey

06/09/2021

HI-2188505

Effect of Cask Spacing on Thermal Performance of HI-

STORM FW System at Point Beach

and 5

HI-2188506

Point Beach Time Histories

HI-2188517

Point Beach SFP Top Floor Level Time Histories

HI-2188657

Point Beach Haul Path Underground Utility Evaluation

HI-2188752

Cask Handling Weights at Point Beach Nuclear Plant

HI-2188838

Seismic Analysis of Cask Loading Area

HI-2188848

Stability Analysis of HI-TRAC VW on Cask Decontamination

Area During Seismic Event

and 5

HI-2200094

Thermal Evaluation of HI-TRAC VW in Decontamination

Area

2, 3, and 5

HI-2200202

Point Beach Site Boundary Dose Rates Calculations for

HI-STORM FW System

HI-2200204

HI-STORM FW and HI-TRAC VW CoC Dose Rate

Calculations for Point Beach

HI-2200225

Seismic Analysis of Spent Fuel Rack Storage Assembly for

Point Beach

HI-2200436

Seismic Stability Analysis of HI-STORM/HI-TRAC Stack

During MPC Transfer Operations

HI-2200438

Evaluation of Transporter Fire Effects on HI-STORM FW and

HI-TRAC VW at Point Beach

HI-2200572

Structural Analysis of the Truck Bay Floor Slab During

Stack-Up Loading

HI-2200631

Evaluation of Plant Hazards at Point Beach Nuclear Plant

HI-2200744

Seismic Analysis of the Hi-STORM on Hauling Transporter

and 3

HI-2200849

VCT Seismic Stability at Point Beach Nuclear Plant (PBNP)

and 5

Calculations

HI-2201043

Structural Evaluation of HI-STORM FW XL Mating Device

60856

Corrective Action

Documents

AR 02385941

21 ISFSI Inspection Question 1, Calculation Revision

Misalignment

03/04/2021

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Resulting from

Inspection

AR 02385944

21 ISFSI Inspection Question 2, Clarify HI-2188505

03/04/2021

CFR 50.59

Screen 2020-

0085

HI-STORM FW Cask System Licensing and Operations

EC 293950

Document Change Request Form

EC 294399

Cask Decontamination Platform Modification

EC 294400

Holtec ISFSI Expansion - Temperature Monitoring System

EC 294818

HI-STORM FW Cask System Licensing and Operation

ECO-5018-118

Limits of Storage Overpack Steel

Holtec 10 CFR 2.48 Evaluation

No.: 1472

ECO-5018-118

Holtec 10 CFR 2.48 Evaluation

No.: 1518

Transition of Spent Fuel Storage for Point Beach Nuclear

Plant

Engineering

Changes

Holtec 10 CFR 2.48 Evaluation

No.: 1529

Foreign Materials

RRTI 2951-001

PBNP Non-Mechanistic Tipover

RRTI 2951-002

PBNP ISFSI Pad Structural Assessment

RRTI 2951-005

Tornado Missile

RRTI 2951-006

Blast Pressure Wave

RRTI 2951-007

Spent Fuel Water Displacement When the HI-TRAC is

Placed Inside the Pool

RRTI 2951-008

Ancillary Equipment Combustibles

Engineering

Evaluations

RRTI 2951-010

Transformers Along Haul Path

Miscellaneous

10CFR50.54(q)(2) - Maintaining the Emergency Plan

Evaluation Form

Radiation

Surveys

ATI Report No.:

8006-100-1422-A

1st Quarter, 2021, TLDs

05/19/2021

Miscellaneous

PBF-2124a

Mean Converted Lake Level Calculation

AOP-13C

Severe Weather Conditions

71111.01

Procedures

NP 2.1.5

Electrical Communications, Switchyard Access and Work

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Planning

NP 8.4.17

PBNP Flooding Program

PBNP-MISO-

NUC-001

Nuclear Plant Operating Agreement for Point Beach Nuclear

Plant

110E017 Sheet 1

P&ID Safety Injection System, Unit 1

110E017 Sheet 2

P&ID Safety Injection System, Unit 1

110E017 Sheet 3

P&ID Safety Injection System, Unit 1

M 217 Sheet 3

P&ID Auxiliary Feedwater System, Unit 1

Drawings

M-217 Sheet 1

P&ID Auxiliary Feedwater System, Units 1 & 2

2

CL 13E Part 2

Auxiliary Feedwater Valve Lineup Motor Driven

71111.04

Miscellaneous

CL 7A

Safety Injection System Checklist Mode 1,2,3 Unit 1

AR 2391043

PFP-0-PAB 8 - Pre-Fire Plan Primary Auxiliary (In Drawing)

04/23/2021

Corrective Action

Documents

Resulting from

Inspection

AR 2391044

NRC RI Questions

04/23/2021

PFP-0-CB

Pre-Fire Plan Control Building Elev 8 ft, 26 ft, 44 ft and 66 ft

PFP-0-PAB 26

Pre-Fire Plan Unit 1 & Unit 2 Auxiliary Building 26 FT

PFP-0-PAB 46

Pre-Fire Plan Unit 1 & Unit 2 Auxiliary Building 46 ft

Fire Plans

PFP-0-PAB-8

Primary Auxiliary Building Elevations 8' and Below

Hourly Fire Round Performance Sheet-PAB

04/23/2021

Fire Round Performance Sheet - Turbine Hall and

Miscellaneous Areas

04/06/2021

Miscellaneous

Fire Round Performance Sheet - PAB

04/23/2021

WO 40727584-01

Perform Maintenance on the SCBA

03/27/2021

WO 40731640-01

Perform Maintenance on the SCBA

04/24/2021

71111.05

Work Orders

WO 40735643-01

Perform Maintenance on the SCBA

05/22/2021

Miscellaneous

PBN LOC 21C

001E

NRC Annual Simulator Exam

IT 45 Train B

Safety Injection Valves Train B Unit 2

71111.11Q

Procedures

OP 2D Unit 1

Power Operation Maneuvering - Unit 1

AR 2383251

Unit 2 - Received PPCS Priority Alarm for RTO

2/07/2021

AR 2385451

Unit 2 Invalid LEFM RTO Inputs Causing TLCO Entry

2/28/2021

71111.12

Corrective Action

Documents

AR 2386313

Spike Down on LEFM

03/09/2021

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

AR 2387389

Unexpected PPCS Alarms Due To F-3110, LEFM FW Flow

Spike

03/19/2021

AR 2387460

Unit 1 RTO Shifted to Venturi

03/21/2021

AR 2388057

PBNP LEFM FIP Action - Revise CTC Software Version

03/26/2021

AR 2389030

Trend: LEFM Flow Low Spike Causing False Power

Indication

04/06/2021

Miscellaneous

EVAL-PB-GT-

2402

G-05 Gas Turbine Exceeded Reliability (FF) Criteria

05/28/2021

Corrective Action

Documents

Resulting from

Inspection

2392117

NRC Identified Incorrect PDC Noted in Look Ahead

05/03/2021

High Risk Plan for 2DY-02, 125V DC / 120V AC Inverter

Maintain and Inspect

05/04/2021

PBNP Shutdown Safety Assessment and Fire Inspection

Checklist

06/28/2021

PBNP Shutdown Safety Assessment and Fire Inspection

Checklist

06/29/2021

T-0 Execution Schedule by Early Start

06/28/2021

T-0 Execution Schedule by Early Start

06/29/2021

T-0 Execution Schedule by Early Start

06/30/2021

Risk Plan for 1ICP 2.5B -- Safeguards Logic Test - Train B

04/15/2021

Miscellaneous

Risk Plan for 1ICP 2.3B -- Reactor Protection Logic

Test - Train B

04/15/2021

Procedures

NP 10.3.7

On-Line Safety Assessment

WO 40770258-01

1ICP 2.3B - RP Logic Test - Train B

04/15/2021

71111.13

Work Orders

WO 40770259-01

1ICP 2.5B - SG Logic Test - Train B

04/15/2021

AR 2385693

Potential Thru Wall Leak on CCW Identified

03/02/2021

AR 2386041

PPG AC 0152N-11 Unit 2 NDE Periodic Monitoring

03/05/2021

AR 2386499

CCW Piping Analysis not Updated for Removed Pipe

Penetration

03/10/2021

AR 2388991

NRC Identified Pipe Hanger Moved from Original Location

04/06/2021

71111.15

Corrective Action

Documents

AR 2389208

2P-29 (TDAFP) Elevated Temp on Pump Inbd Packing

Gland

04/08/2021

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

AR 2395115

Increased Frequency of Nitrogen Addition to PORV

Accumulator

06/06/2021

Corrective Action

Documents

Resulting from

Inspection

AR 2395643

Code Case Required Inspection of U2 CCW Pipe Not

Performed

06/10/2021

295970

Nonplanar Flaw Evaluation in CCW Piping Adjacent to

2CC-753

Engineering

Changes

296054

Piping Analysis of CCW Return Piping for Removed

Penetration to Support POD 02386499-01

Operability

Evaluations

AR 2386499-01

CCW Piping Analysis Not Updated for Removed Pipe

Penetration

03/24/2021

Work Orders

WO 40767858-01

2PPG AC 0152N-11/Unit 2 NDE Periodic Monitoring

03/24/2021

WO 40662293-01

1-62-2/A-06 Relay Replacement

04/29/2021

WO 40685444-01

1A-06 Calibrate 1A-06 Tech Spec Relays

05/03/2021

WO 40727871-01

K-002B-18 Month Compressor Maintenance

04/09/2021

WO 40727871-02

K-002B-18 Month Compressor Maintenance

04/09/2021

WO 40732255-01

2DY-02 - Maintain and Inspect Inverter

05/04/2021

WO 40757762-01

1-62-1/A-06 Relay Replacement

04/29/2021

71111.19

Work Orders

WO 407702260-

G-05/Abnormal Indications on G-05 HMI

04/05/2021

Corrective Action

Documents

Resulting from

Inspection

AR 2396818

Criteria Specified in 0-SOP-FLEX-003 Not Direct Correlation

06/24/2021

IT 07D

P-32D Service Water Pump (Quarterly)

IT 07E

P-32E Service Water Pump (Quarterly)

IT 07F

P-32F Service Water Pump (Quarterly)

Procedures

TS 83

Emergency Diesel Generator G-03 Monthly

WO 40614014-01

IT-07D, P-32D Service Water Pump Comprehensive Test

05/22/2019

WO 40728667-01

IT 45 Train B, Unit 2 Safety Injection VLVS

04/08/2021

WO 40730667-01

IT-08A, 1P-29 AFP Cold Start Test/VLVS

04/19/2021

WO 40730691-01

TS-81, G-01 Emergency Diesel Generator Operability

04/18/2021

71111.22

Work Orders

WO 40734042-01

IT-07D, P-32D Service Water Pump Comprehensive Test

05/12/2021

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

WO 40734388-01

IT-07E, P-32E Service Water Pump Comprehensive Test

05/12/2021

WO 40734389-01

IT-07F, P-32F Service Water Pump Comprehensive Test

05/12/2021

WO 40735866-01

0-SOP-FLEX-003 / Z-2003A and B Annual Full Flow Tests

06/02/2021

Drill Scenario

04/28/2021

Nuclear Accident Reporting Form

04/28/2021

NPM # 2019-

0035

1Q19 EP Drill Report

03/21/2019

NPM # 2019-

0102

4Q19 EP Drill Report

11/04/2019

71114.06

Miscellaneous

NPM # 2021-

0048

2Q21 EP Drill Report

05/25/2021

20-1016

Remove/Reinstall RV Head

Various

20-1025

Scaffolding Containment Outage Activities

Various

ALARA Plans

20-1062

RCS Leak Repair

Various

N/A

Point Beach U1R39 Radiation Protection Post Outage

Report

Miscellaneous

N/A

Point Beach U2R37 Radiation Protection Post Outage

Report

Procedures

NISP-RP-010

Radiological Job Coverage

20-1016

Remove/Reinstall RV Head

20-1025

Scaffolding Containment Outage Activities

71124.02

Radiation Work

Permits (RWPs)

20-1062

RCS Leak Repair

Corrective Action

Documents

AR 2294511-66

Evaluate New Fit Testing Method for Possible

Implementation

N/A

Corrective Action

Documents

Resulting from

Inspection

AR 2391216

SCBA Discrepancies Identified

04/26/2021

Procedures

PC 75 Part 1

Monthly and Turnaround Maintenance for The Scott 4.5

Self-Contained Breathing Apparatus

AR 2329355-04

L1A/L2A/RWT: AR02381669, Level 1 NRC IP 71124.03 and

71124.04 Inspection Assessment

01/22/2021

Self-Assessments

AR 2337124-03

Annual RP Program Review

03/10/2020

71124.03

Work Orders

WO 40523755 01

18-Month Filter Testing

10/08/2018

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

WO 40625100 01

18-Month Filter Testing

04/15/2020

Corrective Action

Documents

AR 2330629

Individual Handled a Source Without Dosimetry

11/19/2019

HP-100-091219

R0

Plant Source Term and Impact on RP Program

09/12/2019

ID No.

JDG01UAW

Whole Body Count Evaluation

10/12/2020

Miscellaneous

NVLAP Lab

Code: 100555-0

Certificate of Accreditation to ISO.IEC 17025:2017

06/30/2021

HPIP 1.12

Bioassay Requirements

HPIP 1.57.1

Evaluation of Whole Body Count Results

HPIP 1.65

Personnel Neutron Exposure Monitoring

HPIP 1.66

Dosimetry Placement for Extremity and Multiple Whole Body

Locations and Extremity Dose Determination

NP 4.2.15

Fetal Protection Policy Implementation

NP 4.2.27

Personnel Exposure Monitoring Device Minimum

Requirements and General Use

Procedures

RP-AA-101

Personnel Monitoring Program

71124.04

Self-Assessments AR 2329342-04

L1A/L2A/RWT: 02369603, Level 1 NRC Baseline RP

Inspection Assessment

09/25/2020

AR 2323824

Environmental Samples Below Minimum Volume

09/11/2019

AR 2358450

Isotope Half-life Study to Determine Unidentified Peak

2/21/2020

AR 2367804

2nd Quarter Facade Well Sample Required LLD Not Met

09/14/2020

Corrective Action

Documents

AR 2368172

August GW Samples Could Not be Obtained

09/16/2020

AR 2396572

2016 AMR Liquid Dose Update

06/22/2021

AR 2396703

GWPP Enhancement for Warehouse 7 SSC

06/23/2021

Corrective Action

Documents

Resulting from

Inspection

AR 2396822

REMP Air Station Housing Units Review

06/24/2021

Updated Site Conceptual Model

01/01/2017

ACIT 0337720-01

Evaluate REMP Samples for Potential Reduction

Not Provided

NRC 2020-009

2019 Annual Monitoring Report

04/27/2020

NRC 2021-0021

20 Annual Monitoring Report

04/29/2021

71124.07

Miscellaneous

ODCM

Offsite Dose Calculation Manual

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Report Number

2019-001

Chesapeake

Nuclear Services

Point Beach Nuclear Power Plant Meteorological and

Atmospheric Dispersion Report

07/19/2019

HPIP 3.58.1

Radiological Environmental Sampling

NP 3.4.7

Groundwater Protection Program (GWPP)

Procedures

NP 3.4.9

Groundwater Protection Plan Technical Basis

Self-Assessments NEI 07-07 Peer

Assessment

Report

NEI Ground Water Protection Initiative

2/15/2017

WO 40313947-02

Supplement

Meteorological Tower Inspection Reports

06/30/2016

WO 40689482 02

ICP 6.3-2 -- Meteorological System Calibration

08/25/2020

Work Orders

WO 40727734 01

ICP 7.30 - Inspection of Meteorological Sites

06/10/2021

Performance Indicators; Units 1 and 2; Reactor Coolant

System Leakage

04/01/2020 -

03/31/2021

Miscellaneous

Performance Indicators; Units 1 and 2; Safety System

Functional Failures

04/30/2020 -

03/31/2021

LI-AA-100-10003

NRC Performance Indicator

71151

Procedures

NP 5.2.16

NRC Performance Indicators

2012-0006

Service Water Flow during NFPA 805 Fire Events

2018-0016

Service Water Flow during NFPA 805 Fire Events

FPTE 2016-003

PBN Nuclear Safety Capability Assessment (NSCA)

Calculations

PRA 8.1

Fire PRA Plant Boundary Definition and Partitioning

Notebook

AR 02286581

NFPA 805 Documentation Incorrect

10/18/2018

AR 02331840

NFPA 805 Action Not Contained in Procedure

10/17/2019

Corrective Action

Documents

AR 02331854

NFPA 805 Spurious Operation of Service Water Valves Not

Considered

10/17/2019

Corrective Action

Documents

Resulting from

Inspection

AR 2395628

NRC Identified Small Gap in Barrier Between FZ 245 and

FZ 322

06/10/2021

71152

Procedures

EOP-2 UNIT 1

Faulted Steam Generator Isolation

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

OM 3.27

Control of Fire Protection and NFPA 805 Equipment

77