ML18017A931: Difference between revisions

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{{#Wiki_filter:REGULATORY ORMATION DISTRIBUTION SY f (RIDS)ACCESSION NBR!8003030612
{{#Wiki_filter:REGULATORY         ORMATION DISTRIBUTION SY         f (RIDS)
, DOC CHOATE: 80/02/22 NOTARIZED!
CHOATE:
NO FACIL:50-400 Shearon Harris Nuclear Power Plant~Unft ig Caroljna 50 401 Shearon Harrjs Nuclear Power Plant~Unit 2~Carolfna 50 402 Shearon Harris Nuclear Power Planti Unft 3g Carolina AUTH'AME AUTHOR AFFILIATION CHIANGIiN.J.
ACCESSION NBR!8003030612                     ,
Carolina Power 3 Light Co~, RECIP~NAME RECIPIENT AFFILIATION DOCKET 0 05000400 05000401 05000402+o3'UBJECT:
DOC         80/02/22     NOTARIZED!   NO       DOCKET 0 FACIL:50-400 Shearon Harris Nuclear Power Plant~ Unft ig Caroljna                               05000400 50 401 Shearon Harrjs Nuclear Power Plant~ Unit 2~ Carolfna                           05000401 50 402 Shearon Harris Nuclear Power Planti Unft 3g Carolina                           05000402 AUTH'AME                           AUTHOR AFFILIATION CHIANGIiN.J.                       Carolina   Power 3 Light Co ~,
Final rept on defective Seismic Class I" hangar weld'o longer considered reportable under 10CFR50~55(e)~Metallurgical investigation revealed basically cosmetic defects'orrective actions completed L a'cceptable
RECIP ~ NAME                       RECIPIENT AFFILIATION
~DISTRIBUTION CODE l SO I9S COPIES RECEIYED>LTR l ENCL.SIZE:~TITLE'.Construction Deficiency Report (10CFR50.55E)
                                                                                                        +o3'UBJECT:
FT'P NOTES~RECIPIENT'D CODE/NAME ACT'ION!14 PM 20 LA LGcJg W~INTERNAL: 0 G RILE 05 IL 08 MPA 10 GAB 12 JORDAN'/IE~
Final rept             on defective Seismic Class I" hangar weld'o longer considered reportable under 10CFR50 55(e)               ~       ~
16 AD FOR ENGR ,17 AD REAC'FTY 23 OELD AEOD GEOSCIKNCES BR ISC SYS BR MECH ENG BR STRUCT'NG BR EXTERNAL: 03 LPDR 24 ACRS COPIES LXTR ENCL 1 1 1 1 1 1 2, 2'1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 16 16'ECIPIENT IO CODE/NAME 15 BC 21 AO 02 NRC PDR 07 EDO L STAFF 09 DEPY DIR DPM ii STANDRDS OEV 13F IELD COOR/IE'7 AD PLANT SYS 22 DIR DPM AO/SI TE TECH DIRECTOR OSE" HANAUERiS~MATL, KNG BR PO>IER SYS BR 04 NSIC COPIES LTTR ENCL'1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 LA-Wydg E KE'BLu sa.~E/8'M LA TOTAL NUMBER Of COPIES REQUIRED: LTTR M ENCL' I 1" l f 4 e I l I l M II 4 g K~~II l/W lg q ll P nr g h, p I i(N g I)I FORM 21~1OOM Pebruary 22, 1980 Caroiina Power&Light Company Raleigh, N.C.2?602 P D Mr.James P.O'ReiU.y United States Nuclear Regulatory Commission Region XI 101 Marietta Street, Northwest Atlanta, Georgia 30303 SHEARON HARRIS NUCLEAR POWER PLANT UNITS 1, 2, 3, 6 4 DOCKET NOS~50-400, 50-401, 50-402, 50-403 DEPECTIVE SEISMIC CLASS X HANGER WELDS, OPEN ITEM 400/401 79<<23-05
Metallurgical investigation revealed basically cosmetic defects'orrective actions completed L a'cceptable                       ~
DISTRIBUTION CODE l TITLE'.
SO I9S   COPIES RECEIYED>LTR       l ENCL.
Construction Deficiency Report (10CFR50.55E)
SIZE:~
FT' NOTES   ~                     P RECIPIENT'D                   COPIES          'ECIPIENT              COPIES CODE/NAME          LXTR ENCL        IO CODE/NAME         LTTR ENCL' ACT'ION!       14 PM                               1      1      15 BC                          1 20 LA LGcJg             W~         1      1      21 AO                      1    1 INTERNAL:     0               G   RILE           1      1      02 NRC PDR                1    1 05 IL                               2,    2'    07 EDO L STAFF            1    1 08 MPA                                           09 DEPY DIR DPM 10 GAB 12 JORDAN'/IE~
1 1
1 1
1 ii  STANDRDS 13F IELD COOR/
OEV 1
1 1
1 IE'7 1   1 16 AD FOR ENGR                      1     1         AD PLANT SYS          1
              ,17 AD REAC'FTY                      1     1     22 DIR  DPM              1   1 23 OELD                              1     1     AO/SI TE TECH             1   1 AEOD                                1     1     DIRECTOR OSE"              1   1 GEOSCIKNCES BR                      1     1     HANAUERiS ~                1   1 ISC SYS              BR            1     1     MATL, KNG BR              1   1 MECH ENG BR                          1     1     PO>IER SYS BR              1   1 STRUCT'NG                BR        1     1 EXTERNAL: 03 LPDR                                        1     04 NSIC                    1   1 24 ACRS                            16    16 LA-Wydg E KE'BLu sa.~
E/8' M LA TOTAL NUMBER Of COPIES REQUIRED: LTTR                         M     ENCL'


==Dear lir.O'Reilly:==
I 1" l            4  e f
On November 26, 1979, CP&L had notified the NRC (?ir.R.Bradley)by telephone that the subject deficiency had been evaluated and considered to be reportable under the provisions of 10CPR50.55(e).
I      l I l
As indicated to the NRC (Mr.R.Bradley)by telephone on Pebruary 19, 1980, further evaluation has now revealed that the subject deHciency is no longer considered reportable under the provisions of 10CPR50.55(e) on the basis that metallurgical investigation indicates that the types of defects noted were basically cosmetic and.considered minor in nature and are not significant enough to cause subsequent failure.Based on the above, Carolina Power 6 Light Company considers this matter closed.Xt should be noted that all corrective action on the subject deficiency has been completed and found to be acceptable.
M    II  4 g K
If you have any quest:iona regarding this matter, please do not hesitate to contact me.KVH/bd (6526)cc: 1Ir.V.Scellc 12)Q Yours very truly, Original Signed By N.i.Chiangi N.J.Chiangi-1ianager Engineering 6 Construction Quality Assurance}}
                                                          ~  ~
II      l  /                                        W lg q ll P
g  h, p  I        N nr i(
g I
                              )I
 
FORM 21 ~ 1OOM D
Caroiina Power & Light Company P
Raleigh, N. C. 2?602 Pebruary 22, 1980 Mr. James P. O'ReiU.y United States Nuclear Regulatory Commission Region XI 101 Marietta Street, Northwest Atlanta, Georgia 30303 SHEARON HARRIS NUCLEAR POWER PLANT UNITS 1, 2, 3, 6 4 DOCKET NOS ~ 50-400, 50-401, 50-402, 50-403 DEPECTIVE SEISMIC CLASS X HANGER WELDS, OPEN ITEM 400/401 79<<23-05
 
==Dear lir. O'Reilly:==
 
On November   26, 1979, CP&L had notified the NRC (?ir. R. Bradley) by telephone that the subject deficiency had been evaluated and considered to be reportable under the provisions of 10CPR50.55(e). As indicated to the NRC (Mr. R. Bradley) by telephone on Pebruary 19, 1980, further evaluation has now revealed that the subject deHciency is no longer considered reportable under the provisions of 10CPR50.55(e) on the basis that metallurgical investigation indicates that the types of defects noted were basically cosmetic and. considered minor in nature and are not significant enough to cause subsequent failure. Based on the above, Carolina Power 6 Light Company considers this matter closed. Xt should be noted that all corrective action on the subject deficiency has been completed and found to be acceptable.
If you   have any quest:iona regarding       this matter, please do not hesitate to contact   me.
Yours very truly, Original Signed By N. i. Chiangi 1ianager KVH/bd    (6526)                                          N. J. Chiangi Engineering 6 Construction cc:  1Ir. V. Scellc  12)Q                                    Quality Assurance}}

Latest revision as of 04:10, 22 October 2019

Final Rept on Defective Seismic Class I Hanger Welds.Welds Not Reportable Under 10CFR50.55(e).Metallurgical Investigation Revealed Basically Cosmetic Defects.Corrective Actions Completed & Acceptable
ML18017A931
Person / Time
Site: Harris  Duke Energy icon.png
Issue date: 02/22/1980
From: Chiangi N
CAROLINA POWER & LIGHT CO.
To: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
References
NUDOCS 8003030612
Download: ML18017A931 (3)


Text

REGULATORY ORMATION DISTRIBUTION SY f (RIDS)

CHOATE:

ACCESSION NBR!8003030612 ,

DOC 80/02/22 NOTARIZED! NO DOCKET 0 FACIL:50-400 Shearon Harris Nuclear Power Plant~ Unft ig Caroljna 05000400 50 401 Shearon Harrjs Nuclear Power Plant~ Unit 2~ Carolfna 05000401 50 402 Shearon Harris Nuclear Power Planti Unft 3g Carolina 05000402 AUTH'AME AUTHOR AFFILIATION CHIANGIiN.J. Carolina Power 3 Light Co ~,

RECIP ~ NAME RECIPIENT AFFILIATION

+o3'UBJECT:

Final rept on defective Seismic Class I" hangar weld'o longer considered reportable under 10CFR50 55(e) ~ ~

Metallurgical investigation revealed basically cosmetic defects'orrective actions completed L a'cceptable ~

DISTRIBUTION CODE l TITLE'.

SO I9S COPIES RECEIYED>LTR l ENCL.

Construction Deficiency Report (10CFR50.55E)

SIZE:~

FT' NOTES ~ P RECIPIENT'D COPIES 'ECIPIENT COPIES CODE/NAME LXTR ENCL IO CODE/NAME LTTR ENCL' ACT'ION! 14 PM 1 1 15 BC 1 20 LA LGcJg W~ 1 1 21 AO 1 1 INTERNAL: 0 G RILE 1 1 02 NRC PDR 1 1 05 IL 2, 2' 07 EDO L STAFF 1 1 08 MPA 09 DEPY DIR DPM 10 GAB 12 JORDAN'/IE~

1 1

1 1

1 ii STANDRDS 13F IELD COOR/

OEV 1

1 1

1 IE'7 1 1 16 AD FOR ENGR 1 1 AD PLANT SYS 1

,17 AD REAC'FTY 1 1 22 DIR DPM 1 1 23 OELD 1 1 AO/SI TE TECH 1 1 AEOD 1 1 DIRECTOR OSE" 1 1 GEOSCIKNCES BR 1 1 HANAUERiS ~ 1 1 ISC SYS BR 1 1 MATL, KNG BR 1 1 MECH ENG BR 1 1 PO>IER SYS BR 1 1 STRUCT'NG BR 1 1 EXTERNAL: 03 LPDR 1 04 NSIC 1 1 24 ACRS 16 16 LA-Wydg E KE'BLu sa.~

E/8' M LA TOTAL NUMBER Of COPIES REQUIRED: LTTR M ENCL'

I 1" l 4 e f

I l I l

M II 4 g K

~ ~

II l / W lg q ll P

g h, p I N nr i(

g I

)I

FORM 21 ~ 1OOM D

Caroiina Power & Light Company P

Raleigh, N. C. 2?602 Pebruary 22, 1980 Mr. James P. O'ReiU.y United States Nuclear Regulatory Commission Region XI 101 Marietta Street, Northwest Atlanta, Georgia 30303 SHEARON HARRIS NUCLEAR POWER PLANT UNITS 1, 2, 3, 6 4 DOCKET NOS ~ 50-400, 50-401, 50-402, 50-403 DEPECTIVE SEISMIC CLASS X HANGER WELDS, OPEN ITEM 400/401 79<<23-05

Dear lir. O'Reilly:

On November 26, 1979, CP&L had notified the NRC (?ir. R. Bradley) by telephone that the subject deficiency had been evaluated and considered to be reportable under the provisions of 10CPR50.55(e). As indicated to the NRC (Mr. R. Bradley) by telephone on Pebruary 19, 1980, further evaluation has now revealed that the subject deHciency is no longer considered reportable under the provisions of 10CPR50.55(e) on the basis that metallurgical investigation indicates that the types of defects noted were basically cosmetic and. considered minor in nature and are not significant enough to cause subsequent failure. Based on the above, Carolina Power 6 Light Company considers this matter closed. Xt should be noted that all corrective action on the subject deficiency has been completed and found to be acceptable.

If you have any quest:iona regarding this matter, please do not hesitate to contact me.

Yours very truly, Original Signed By N. i. Chiangi 1ianager KVH/bd (6526) N. J. Chiangi Engineering 6 Construction cc: 1Ir. V. Scellc 12)Q Quality Assurance