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{{#Wiki_filter: | {{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION REGION III 2443 WARRENVILLE RD. SUIT E 210 LISLE, ILLINOIS 60532 | ||
-4352 January 3, 2018 Mr. David B. Hamilton Site Vice President FirstEnergy Nuclear Operating Company Perry Nuclear Power Plant Reg Affairs | |||
-A210 10 Center Road, P.O. Box 97 Perry, OH 44081 | |||
-0097 | |||
Mr. | SUBJECT: PERRY NUCLEAR POWER PLANT | ||
-NRC DESIGN BASES ASSURANCE INSPECTION (TEAMS) INSPECTION REPORT 05000440/ | |||
2017008 Dear Mr. Hamilton | |||
: On September 14, 2017, the U.S. Nuclear Regulatory Commission (NRC) completed a triennial baseline Design Bases Assurance Inspection (Team s) at your Perry Nuclear Power Plan The enclosed report documents the results of this inspection, which were discussed on November 22, 2017, with Mr. Conicella, and other members of your staf Three NRC-identified findings of very | |||
-low safety significance were identifie The findings involved violation s of NRC requirement However, because of their very-low safety significance, and because the issues were entered into your Corrective Action Program, the NRC is treating the issues as Non-Cited Violations in accordance with Section 2.3.2 of the NRC Enforcement Polic If you contest the violations or significance of these Non-Cited Violations, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555 0001; with copies to the Regional Administrator, Region III; the Director, Office of Enforcement; and the NRC resident inspector at the Perry Nuclear Power Plant | |||
. If you disagree with a cross | |||
-cutting aspect assignment or a finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555 | |||
-0001; with copies to the Regional Administrator, Region III | |||
; and the NRC resident inspector at the Perry Nuclear Power Plan D. Hamilton | |||
-2- This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading | |||
-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, "Public Inspections, Exemptions, Requests for Withholding." | |||
Sincerely,/RA/ Mark T. Jeffers, Chief Engineering Branch 2 Division of Reactor Safety Docket N License No. NPF | |||
-58 | |||
Sincerely,/RA/ Mark T. Jeffers, Chief Engineering Branch 2 Division of Reactor Safety Docket | |||
===Enclosure:=== | ===Enclosure:=== | ||
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=SUMMARY= | =SUMMARY= | ||
Inspection Report 05000440/2017008, 08/14/2017-09/14/2017; Perry Nuclear Power Plant; Design Bases Assurance Inspection (Teams). The inspection was a 2-week onsite baseline inspection that focused on the design of components and modifications to mitigating systems. The inspection was conducted by regional engineering inspectors and two consultants. The inspection team identified three findings of very-low safety significance (Green) associated with Non-Cited Violations (NCVs) of U.S. Nuclear Regulatory Commission (NRC) regulations. The significance of inspection findings is indicated by their color (i.e., Green, White, Yellow, and Red) and determined using Inspection Manual Chapter 0609, "Significance Determination Process," dated April 29, 2015. Cross-Cutting aspects are determined using Inspection Manual Chapter 0310, "Aspects Within the Cross-Cutting Areas," dated December 4, 2014. All violations of NRC requirements are dispositioned in accordance with the NRC's Enforcement Policy, dated November 1, 2016. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 6, dated July 2016. | Inspection Report 05000440/2017008 | ||
, 08/14/2017-09/14/2017; Perry Nuclear Power Plant | |||
; Design Bases Assurance Inspection (Teams). The inspection was a 2 | |||
-week onsite baseline inspection that focused on the design of components and modifications to mitigating systems. The inspection was conducted by regional engineering inspectors and two consultants. The inspection team identified three findings of very-low safety significance (Green) associated with Non-Cited Violations (NCVs) of U.S. Nuclear Regulatory Commission ( | |||
NRC) regulations. The significance of inspection findings is indicated by their color (i.e., Green, White, Yellow, and Red) and determined using Inspection Manual Chapter 0609, "Significance Determination Process | |||
," dated April 29, 2015. Cross-Cutting aspects are determined using Inspection Manual Chapter 0310, "Aspects Within the Cross-Cutting Areas | |||
," dated December 4, 2014. All violations of NRC requirements are dispositioned in accordance with the NRC's Enforcement Policy, dated November 1, 2016. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG | |||
-1649, "Reactor Oversight Process | |||
," Revision 6, dated July 2016 | |||
. | |||
===NRC-Identified=== | ===NRC-Identified=== | ||
and Self-Revealed Findings | and Self-Revealed Findings | ||
===Cornerstone: Mitigating Systems === | ===Cornerstone: Mitigating Systems=== | ||
: '''Green.''' | : '''Green.''' | ||
The team identified a finding of very-low safety significance (Green) and an associated NCV of Title 10 of the Code of Federal Regulations (CFR), Part 50, Appendix B, Criterion III, "Design Control," and 10 CFR 50.63, "Loss of All Alternating Current Power," for the licensee's failure to evaluate the capability to transfer the high pressure core spray (HPCS) and the reactor core isolation cooling (RCIC) pumps' suction source from the condensate storage tank ( | The team identified a finding of very-low safety significance (Green) and an associated NCV of Title 10 of the Code of Federal Regulations (CFR), Part 50, Appendix B, Criterion III, "Design Control," and 10 CFR 50.63, "Loss of All Alternating Current Power," for the licensee's failure to evaluate the capability to transfer the high pressure core spray (HPCS) and the reactor core isolation cooling (RCIC) pumps' suction source from the condensate storage tank (C ST) to the suppression pool during cold weather conditions. Specifically, (1) monitoring of the CST level instrument lines heat tracing was inadequate to detect a credible common mode failure before the instrument lines would freeze and be rendered inoperable during normal operation, (2)the licensee did not address the condensate (CST) level instrument lines susceptibility to freeze during a cold weather loss of off-site power (LOOP) event with or without a design basis transient or accident, and (3) the licensee incorrectly evaluated the capability to transfer the HPCS pump suction source from the CST to th e suppression pool during a cold weather station blackout (SBO) event. The licensee captured the issues within their Corrective Action Program (CAP) as Condition Report (CR) CR-2017-08685, CR | ||
-2017-08930, and CR | |||
-2017-09006. Corrective actions implemented included: | |||
increased the CST level instrument line heat tracing circuit monitoring frequency, revise d the affected procedures ensure d HPCS and RCIC are adequately aligned to the suppression pool during LOOP design basis events, and ensured a timely transfer of the HPCS and RCIC pump suctions to the suppression pool during a SBO. | |||
The performance deficiency was determined to be more-than-minor because it was associated with the Mitigating Systems cornerstone attribute of design control and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. | |||
Specifically, the failure of the HPCS and or RCIC pumps to automatically transfer their suction source from the CST to the suppression pool upon reaching a low CST water level condition could damage the pump(s) thus preventing them to be used to mitigate a transient or accident. | |||
A detailed risk evaluation was performed and determined that the finding was of very-low safety- significance (Green). The team did not identify a cross-cutting aspect associated with this finding because it was not confirmed to reflect current performance due to the age of the performance deficiency. Specifically, the CST instrument lines were designed and the SBO coping strategy during cold weather was established more than years ago. | |||
(Section 1R21.3.b( | |||
1)) | |||
: '''Green.''' | : '''Green.''' | ||
The team identified a finding of very-low safety significance (Green) and an associated NCV of 10 CFR Part 50, Appendix B, Criterion III, "Design Control," for the failure to consider all stresses resulting from the emergency closed cooling system as built pipe support 1P42-H1080 connection details. Specifically, the evaluation for the pipe support did not address the impact of rigid connections at both ends of the W8 steel post and of the lateral load on W21 auxiliary steel beam. The licensee captured the issues in their CAP as CR-2017-08986 and CR-2017-09043, reasonably determined the support remained operable, and planned to revise the affected structural analyses. The performance deficiency was determined to be more-than-minor because it was associated with the Mitigating Systems cornerstone attribute of design control and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the failure to analyze actual pipe configuration and to evaluate the W21 beam did not ensure the emergency closed cooling system and its safety-related supported loads would remain available and capable of providing their accident mitigating function. The finding screened as of very-low safety significance (Green) because it did not result in the loss of operability or functionality of mitigating systems. The team determined that this finding had a cross-cutting aspect in the area of human performance because the licensee did not recognize and plan for the possibility of mistakes, latent issues, and inherent risk, even while expecting successful outcomes. Specifically, the licensee did not recognize this latent issue when revising the structural evaluation in 2015. (Section 1R21.4.b(1)) [H.12] | The team identified a finding of very-low safety significance (Green) and an associated NCV of 10 CFR Part 50, Appendix B, Criterion III, "Design Control," for the failure to consider all stresses resulting from the emergency closed cooling system as built pipe support 1P42 | ||
-H1080 connection details. Specifically, the evaluation for the pipe support did not address the impact of rigid connections at both ends of the W8 steel post and of the lateral load on W21 auxiliary steel beam. The licensee captured the issues in their CAP as CR | |||
-2017-08986 and CR | |||
-2017-09043, reasonably determined the support remained operable, and planned to revise the affected structural analyses. | |||
The performance deficiency was determined to be more-than-minor because it was associated with the Mitigating Systems cornerstone attribute of design control and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. | |||
Specifically, the failure to analyze actual pipe configuration and to evaluate the W21 beam did not ensure the emergency closed cooling system and its safety-related supported loads would remain available and capable of providing their accident mitigating function. The finding screened as of very-low safety significance (Green) because it did not result in the loss of operability or functionality of mitigating systems. The team determined that this finding had a cross-cutting aspect in the area of human performance because the licensee did not recognize and plan for the possibility of mistakes, latent issues, and inherent risk, even while expecting successful outcomes. Specifically, the licensee did not recognize this latent issue when revising the structural evaluation in 2015. | |||
(Section 1R21.4.b(1)) | |||
[H.12] | |||
: '''Green.''' | : '''Green.''' | ||
The team identified a finding of very-low safety significance (Green) and an associated NCV of 10 CFR Part 50, Appendix B, Criterion III, "Design Control," for the failure to verify the capability to manually backwash the emergency service water (ESW) strainer during a LOOP. Specifically, the licensee credited the capability to manually backwash the ESW strainers during a LOOP. However, the associated differential pressure alarm setpoint did not ensure sufficient time to complete this activity because the alarms were set at the same value as the design differential pressure value assumed by the hydraulic calculations. The licensee captured the issue in their CAP as CR-2017-09033, reasonably determined ESW remained operable, and planned to revise the associated calculation and the alarm setpoint to ensure sufficient time to perform the required manual actions during a LOOP. | The team identified a finding of very-low safety significance (Green) and an associated NCV of 10 CFR Part 50, Appendix B, Criterion III, "Design Control," for the failure to verify the capability to manually backwash the emergency service water (ESW) strainer during a LOOP. Specifically, the licensee credited the capability to manually backwash the ESW strainers during a LOOP. However, the associated differential pressure alarm setpoint did not ensure sufficient time to complete this activity because the alarms were set at the same value as the design differential pressure value assumed by the hydraulic calculations. The licensee captured the issue in their CAP as CR-2017-09033, reasonably determined ESW remained operable, and planned to revise the associated calculation and the alarm setpoint to ensure sufficient time to perform the required manual actions during a LOOP. | ||
4 The performance deficiency was determined to be more-than-minor because it was associated with the Mitigating Systems cornerstone attribute of protection against external factors and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the performance deficiency did not assure the ESW capability to supply the required minimum flow to its supported components. The finding screened as of very-low safety significance (Green) because it did not result in the loss of operability or functionality of mitigating systems. The team did not identify a cross-cutting aspect associated with this finding because it was not confirmed to reflect current performance due to the age of the performance deficiency. Specifically, the alarm setpoint was established more than | 4 The performance deficiency was determined to be more-than-minor because it was associated with the Mitigating Systems cornerstone attribute of protection against external factors and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the performance deficiency did not assure the ESW capability to supply the required minimum flow to its supported components. The finding screened as of very-low safety significance (Green) because it did not result in the loss of operability or functionality of mitigating systems. The team did not identify a cross-cutting aspect associated with this finding because it was not confirmed to reflect current performance due to the age of the performance deficiency. Specifically, the alarm setpoint was established more than years ago. (Section 1R21.6.b(2)) | ||
5 | 5 | ||
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==REACTOR SAFETY== | ==REACTOR SAFETY== | ||
Cornerstone s: Initiating Events, Mitigating Systems, and Barrier Integrity | |||
{{a|1R21}} | {{a|1R21}} | ||
==1R21 Design Bases Assurance Inspection ( | ==1R21 Design Bases Assurance Inspection (Team== | ||
s) (71111.21 M) | |||
===.1 Introduction=== | ===.1 Introduction=== | ||
===.2 Inspection Sample Selection Process The team used information contained in the licensee's Probabilistic Risk Assessment and the Perry Nuclear Power Plant Standardized Plant Analysis Risk (SPAR) Model to identify one scenario to use as the basis for component selection. | The objective of the design bases assurance inspection is to verify that design bases have been correctly implemented for the selected risk | ||
The scenario selected was a loss of offsite power (LOOP) event. Based on this scenario, a number of risk-significant components, including those with Large Early Release Frequency (LERF) implications, were selected for the inspection. The team also used additional component information such as a margin assessment in the selection process. This design margin assessment considered original design reductions caused by design | -significant components and modifications, and that operating procedures and operator actions are consistent with design and licensing bases. As plants age, their design bases may be difficult to determine and an important design feature may be altered or disabled during a modification. The inspection also monitors the implementation of modifications to structures, systems, and components as modifications to one system may also affect the design bases and functioning of interfacing systems as well as introduce the potential for common cause failures. The Probabilistic Risk Assessment model assumes the capability of safety systems and components to perform their intended safety function successfully. This inspect able area verifies aspects of the Initiating Events, Mitigating Systems, and Barrier Integrity cornerstones for which there are no indicators to measure performance. | ||
Specific documents reviewed during the inspection are listed in the to the report. | |||
===.2 Inspection Sample Selection Process=== | |||
The team used information contained in the licensee's Probabilistic Risk Assessment and the Perry Nuclear Power Plant Standardized Plant Analysis Risk (SPAR) Model to identify one scenario to use as the basis for component selection. The scenario selected was a loss of offsite power (LOOP) event. Based on this scenario, a number of risk-significant components, including those with Large Early Release Frequency (LERF) implications, were selected for the inspection. | |||
The team also used additional component information such as a margin assessment in the selection process. This design margin assessment considered original design reductions caused by design modification s, power uprates, or reductions due to degraded material condition. Equipment reliability issues were also considered in the selection of components for detailed review. These included items such as performance test results, significant corrective actions, repeated maintenance activities, Maintenance Rule (a)(1) status, components requiring an operability evaluation, system health reports, and U.S. Nuclear Regulatory Commission ( | |||
NRC) resident inspector input of problem areas/equipment. Consideration was also given to the uniqueness and complexity of the design, operating experience, and the available defense in depth 6 margins. A summary of the reviews performed and the specific inspection findings identified are included in the following sections of the report. | |||
The team also identified modifications for review. In addition, the inspectors selected procedures and operating experience issues associated with the selected components. | |||
This inspection constituted 13 samples ( | |||
6 components with 1 component associated with LERF implications, 4 modifications, and 3 operating experience) as defined in Inspection Procedure 71111.21M | |||
-02.01. | |||
===.3 Component Design=== | ===.3 Component Design=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The team reviewed the Updated Final Safety Analysis Report ( | The team reviewed the Updated Final Safety Analysis Report (U FSAR), Technical Specifications, design basis documents, drawings, calculations and other available design basis information, to determine the performance requirements of the selected components. The team used applicable industry standards, such as the American Society of Mechanical Engineers Code, Institute of Electrical and Electronics Engineers Standards | ||
Division 3 Emergency Diesel Generator (EDG) (1E22C0001): The team reviewed the mechanical aspects of the EDG design, including the air starting system, the fuel oil storage and transfer system, and the jacket water cooling system to assess the capability of the EDG to perform its design function under accident and transient conditions. The team reviewed the protection of the EDG and associated equipment from external events, including flooding. The team reviewed the availability of jacket water cooling under LOOP and station blackout (SBO) conditions. The team reviewed the generator circuit diagrams, field winding circuit, grounding scheme, fuel oil transfer pump circuitry, and control logic. The team reviewed the short circuit current calculation data and results, and the coordination calculation to assess the short circuit duty and the coordination between the generator and the motor and transformer loads including ratings and branch circuit cabling. The team also reviewed voltage drop, loading sequence, minimum and maximum voltage profiles, and the impact of the changes in voltage and frequency. The calculation review verified methodology, design inputs, assumptions, and results. The team also reviewed jacket water cooling and air start system test procedures and recent test results. High-Pressure Core Spray (HPCS) Pump (1E22C0001): The team reviewed the following HPCS hydraulic calculations to assess the pump capability to perform its required mitigating functions: pump minimum required flow, runout flow, flow capacity, and minimum required net positive suction head. In addition, the team reviewed the suction sources of the pump and the instrumentation associated with the automatic transfer of the sources. The team reviewed the operation of the HPCS pump under accident, transient, SBO, and external event conditions to assess its capability to perform its licensing basis functions. The team reviewed the room cooling associated with the pump to assess the pump's operating environment. The team reviewed electrical calculations, drawings and equipment modifications to assess the availability of the voltage and current at the pump motor terminals for starting and running under worst case design basis loading, operation on emergency power, and grid voltage conditions. In addition, the team reviewed the control logic, protective relay settings, and cable short circuit current to assess the electrical protection coordination and the power supply feeder cables sizing. The team also reviewed surveillance test procedures and recent test results. Division 2, Safety-Related Instrument Air Containment Isolation Valve (1P57F0015B): The team reviewed the installed configuration of the valve and adjacent pipe supports to verify conformance with the applicable drawings. In addition, the team reviewed the seismic qualification documentation for the valve to assess its seismic qualification; power and control wiring drawings, and voltage drop calculation to assess the availability of the minimum required voltage to the valve under all postulated conditions; and sizing for the cables and fuses. The team also reviewed the system operating procedures, design modifications, maintenance rule documentation, system health reports, periodic 8 maintenance activities, and operability tests, including in-service testing records. This review constituted one component sample with LERF implications. Safety-Related Instrument Air Storage Tank B (1P57A0003B): The team reviewed calculations related to the storage tank capacity, including the minimum allowable pressure and the allowable leakage limits to assess its capacity under the most limiting conditions. The team reviewed seismic anchorage calculation for the tank and the seismic qualification documentation for the instruments. In addition, the team reviewed the associated instrumentation details and the calibration records of the pressure transmitters. The team also reviewed the system operating instructions and testing records. Division 3, 480V Motor Control Centers EF1E-1/2 (1R24S0029/30): The team reviewed the elementary diagram to assess the sizing of control and power fuses and the cables. Also, the voltage drop calculation was reviewed to assess the availability of power and control voltage to the loads and the control components under all postulated conditions. The team also reviewed the design of the associated power supply fuses and the individual load fuses to assess their coordination. HPCS Battery and Charger (1E22S0006 and EFD-1C): The team reviewed calculations and analyses related to battery loads, battery and charger sizing and capacity, hydrogen generation, and battery room temperature. The review was performed to assess the battery and charger capability to support the design basis required voltage requirements of the 125 Vdc Division 3 safety-related loads under both normal and design basis accident conditions. The team also reviewed a sample of completed surveillance tests, service duty discharge tests, and modified performance tests. | , and the National Electric Code, to evaluate acceptability of the systems' design. The NRC also evaluated licensee actions, if any, taken in response to NRC issued operating experience, such as Bulletins, Generic Letters, Regulatory Iss ue Summaries, and Information Notices (INs). The review was to verify that the selected components would function as designed when required and support proper operation of the associated systems. The attributes that were needed for a component to perform its required function included process medium, energy sources, control systems, operator actions, and heat removal. The attributes to verify that the component condition and tested capability was consistent with the design bases and was appropriate may have included installed configuration, system operation, detailed design, system testing, equipment and environmental qualification, equipment protection, component inputs and outputs, operating experience, and component degradation. | ||
For each of the components selected, the inspectors reviewed the maintenance history, preventive maintenance activities, system health reports, operating experience | |||
-related information, vendor manuals, electrical and mechanical drawings, operating procedures, and licensee | |||
's Corrective Action Program (CAP) documents. Field walkdowns were conducted for all accessible components selected to assess material condition, including age-related degradation, configuration, potential vulnerability to hazards, and consistency between the as | |||
-built condition and the design. In addition, the team interviewed licensee personnel from multiple disciplines such as operations, engineering, and maintenance. Other attributes reviewed are included as part of the scope for each individual component. | |||
The following six components (samples), including a component with LERF implications, were reviewed | |||
: | |||
Division 3 Emergency Diesel Generator (EDG) (1E22C0001) | |||
: The team reviewed the mechanical aspects of the EDG design, including the air starting system, the fuel oil storage and transfer system, and the jacket water cooling system to assess the capability of the EDG to perform its design function under accident and transient conditions. The team reviewed the protection of the EDG and associated equipment from external events, including flooding. The team reviewed the availability of jacket water cooling under LOOP and station blackout (SBO) conditions. The team reviewed the generator circuit diagrams, field winding circuit, grounding scheme, fuel oil transfer pump circuitry, and control logic. The team reviewed the short circuit current calculation data and results, and the coordination calculation to assess the short circuit duty and the coordination between the generator and the motor and transformer loads including ratings and branch circuit cabling. The team also reviewed voltage drop, loading sequence, minimum and maximum voltage profiles, and the impact of the changes in voltage and frequency. The calculation review verified methodology, design inputs, assumptions, and results. | |||
The team also reviewed jacket water cooling and air start system test procedures and recent test results. | |||
High-Pressure Core Spray (HPCS) Pump (1E22C0001) | |||
: The team reviewed the following HPCS hydraulic calculations to assess the pump capability to perform its required mitigating functions: pump minimum required flow, runout flow, flow capacity, and minimum required net positive suction head. In addition, the team reviewed the suction sources of the pump and the instrumentation associated with the automatic transfer of the sources. The team reviewed the operation of the HPCS pump under accident, transient, SBO, and external event conditions to assess its capability to perform its licensing basis functions. The team reviewed the room cooling associated with the pump to assess the pump's operating environment. The team reviewed electrical calculations, drawings and equipment modifications to assess the availability of the voltage and current at the pump motor terminals for starting and running under worst case design basis loading, operation on emergency power, and grid voltage conditions. In addition, the team reviewed the control logic, protective relay settings, and cable short circuit current to assess the electrical protection coordination and the power supply feeder cables sizing. | |||
The team also reviewed surveillance test procedures and recent test results. | |||
Division 2 | |||
, Safety-Related Instrument Air Containment Isolation Valve (1P57F0015B): The team reviewed the installed configuration of the valve and adjacent pipe supports to verify conformance with the applicable drawings. In addition, the team reviewed the seismic qualification documentation for the valve to assess its seismic qualification; power and control wiring drawings, and voltage drop calculation to assess the availability of the minimum required voltage to the valve under all postulated conditions; and sizing for the cables and fuses. The team also reviewed the system operating procedures, design modifications, maintenance rule documentation, system health reports, periodic 8 maintenance activities, and operability tests, including in-service testing records. | |||
This review constituted one component sample with LERF implications. | |||
Safety-Related Instrument Air Storage Tank B (1P57A0003B): The team reviewed calculations related to the storage tank capacity, including the minimum allowable pressure and the allowable leakage limits to assess its capacity under the most limiting conditions. The team reviewed seismic anchorage calculation for the tank and the seismic qualification documentation for the instruments. In addition, the team reviewed the associated instrumentation details and the calibration records of the pressure transmitters. The team also reviewed the system operating instructions and testing records. | |||
Division 3, 480V Motor Control Centers EF1E-1/2 (1R24S0029/30): The team reviewed the elementary diagram to assess the sizing of control and power fuses and the cables. Also, the voltage drop calculation was reviewed to assess the availability of power and control voltage to the loads and the control components under all postulated conditions. The team also reviewed the design of the associated power supply fuses and the individual load fuses to assess their coordination. | |||
HPCS Battery and Charger (1E22S0006 and EFD | |||
-1C): The team reviewed calculations and analyses related to battery loads, battery and charger sizing and capacity, hydrogen generation, and battery room temperature. The review was performed to assess the battery and charger capability to support the design basis required voltage requirements of the 125 Vdc Division 3 safety | |||
-related loads under both normal and design basis accident conditions. | |||
The team also reviewed a sample of completed surveillance tests, service duty discharge tests, and modified performance tests. | |||
====b. Findings==== | ====b. Findings==== | ||
(1) Failure to Address the Susceptibility of the Condensate Storage Tank Low Level Instrument Lines to Freeze | (1) Failure to Address the Susceptibility of the Condensate Storage Tank Low Level Instrument Lines to Freeze Introduction | ||
: The team identified a finding of very | |||
-low safety significance (Green)and an associate d Non-Cited Violation ( | |||
NCV) of Title 10 of the Code of Federal Regulations (CFR), Part 50, Appendix B, Criterion III, "Design Control," and 10 CFR 50.63, "Loss of All Alternating Current Power," for the licensee's failure to evaluate the capability to transfer the HPCS and the reactor core isolation cooling (RCIC) pumps' suction source from the condensate storage tank (CST) to the suppression pool during cold weather conditions. Specifically, (1) monitoring of the CST level instrument lines heat tracing was inadequate to detect a credible common mode failure before the instrument lines would freeze and be rendered inoperable during normal operation, (2) the licensee did not address the condensate (CST) level instrument lines susceptibility to freeze during a cold weather LOOP event with or without a design basis transient or accident, and (3) the licensee incorrectly evaluated the capability to transfer the HPCS pump suction source from the CST to the suppression pool during a cold weather station blackout (SBO) event. | |||
9 Description | |||
The | : The CST low level instruments are relied upon to transfer the suctions of HPCS and RCIC to the suppression pool before CST water level would result in inadequate submergence (i.e., inadequate net positive suction head and/or vortexing). | ||
The CST level instruments are controlled under Technical Specification 3.3.5.1, "Emergency Core Cooling Instrumentation | |||
," and are credited in the SBO analysis to ensure that an assumed volume of water from the CST is added to the suppression pool to manage suppression pool heat up during the licensed 4 hour coping period without preferred or emergency power. The instrument lines are exposed to the outside environment and rely on heat tracing and insulation to prevent freezing during cold weather conditions. The heat tracing circuit is not safety | |||
-related and not powered by the emergency power sources. | |||
The team identified the following three examples were the licensee did not address the susceptibility of the CST low level instrument lines to freeze affecting the capability to transfer HPCS and RCIC pumps' suction from the CST to the suppression pool under various cold weather conditions: | |||
The team identified that the licensee failed to address the susceptibility of the CST low level lines to freeze during normal operating conditions | |||
. Specifically, the instrument lines heat tracing circuits were susceptible to common mode failure since the circuits were connected to the same electrical cabinet and the expected time to freeze the instrument lines (e.g., less than 90 minutes in some cases) was significantly shorter than the periodic operator rounds (e.g., every 12 hours in most cases)that include verifying that the heat trace circuit is operating properly. Thus, the monitoring of the heat tracing circuit was, therefore, inadequate to ensure that the HPCS and RCIC pump suctions were capable to transfer from the CST to the suppression pool during cold weather because the monitoring frequency would not result in the timely detection of a heat trace circuit failure before a loss of function could occur | |||
. The team identified that the licensee failed to address the susceptibility of the CST low level instrument lines to freeze during design basis LOOP conditions. Specifically, the design did not recognize that the CST level instrument lines would not support HPCS and RCIC suction transfer during a LOOP with cold weather because the heat tracing were not powered by the E DGs. | |||
The team identified that the evaluation of the SBO coping strategy was not technically correct because it non | |||
-conservatively estimated the times to freeze the CST low level instrument lines and transfer the HPCS suction. In this case, the licensee had previously recognized that the design of the CST low level instrument lines would not prevent freezing during an SBO with cold weather because the insulated lines were exposed to the outside environment and their heat trace circuit would not be powered during an SBO. As a result, the licensee developed an SBO coping strategy intended to protect the HPCS and RCIC pumps from inadequate submergence by transferring the entire CST usable volume to the suppression pool before the CST level instrument lines would freeze. This transfer included both the normal transfer through the vessel duri ng normal post reactor trip operations to maintain reactor vessel water level as well 10 as an expedited operation to transfer the CST directly to the suppression pool when reactor vessel makeup was not necessary. This transfer would result in an automatic HPCS and RCIC pump suction swap from the CST to the suppression pool upon reaching a low CST water level | |||
. While the SBO coping analysis only credited HPCS, the plant's procedures treated the RCIC system as the preferred system. However, the team identified that | |||
: The time allotted for pump suction transfer from the CST to the suppression pool was based on a calculation that assumed the instruments remained functional with a small active water volume that was judged by the team to be inadequate. Specifically, the calculation determined the time to freeze the 3/8 inch outside diameter instrument line such that the unfrozen diameter is 1/16 inch (i.e., the unfrozen 1/16 inch core was credited to sense CST level). The 1/16 inch unfrozen diameter was judged by the team to be inadequate because the mathematical model was based on ideal and uniform assumptions that were not applicable to the actual field configuration exposed to non-controlled environmental conditions. In addition, the existence of a relatively small dimension deviation from the assumed dimension value (e.g., an elbow, valve internals, kink on the line, slight deformation due to handling) could exist leading to a freeze seal prior to the estimated freezing time. This non | |||
-conservatism was further exacerbated by significant calculational errors. Specifically, the calculation assumed the instrument lines were perfectly insulated. However, the team identified during a field walk down that the actual insulation was crushed adversely affecting the calculation assumptions regarding insulation thickness and thermal conductivity values. In addition, the calculation did not consider uninsulated valves and angle iron supports extending out of the insulation acting as heat transfer fins which would bypass the insulation | |||
. The evaluation of this strategy underestimated the time to transfer the entire CST usable volume and the pumps' suctions to the suppression pool. Specifically, the licensee estimated that this transfer would occur around 30 | |||
-40 minutes after the SBO initiation. The licensee considered this timeframe acceptable because they estimated (non | |||
-conservatively as previously discussed) about 83 and 106 minutes to freeze the instrument line assuming ambient temperatures of | |||
-10 degrees Fahrenheit and 0 degrees Fahrenheit, respectively. However, the team noted the transfer time was estimated using less than the usable CST volume instead of the entire CST usable volume as directed by plant procedures. The team estimated that the transfer of the entire CST usable volume would take approximately 93 minutes based on a reasonable extrapolation of a scenario the team observed at the control room simulator. | |||
The licensee captured the issues within their CAP as Condition Report ( | |||
CR) CR-2017-08685, CR | |||
-2017-08930, and CR | |||
-2017-09006. Planned corrective actions to be implemented during the next cold weather condition included: an action to increase the CST level instrument line heat tracing circuit monitoring frequency, revise the affected procedures to ensure HPCS and RCIC are adequately aligned to the 11 suppression pool during LOOP design basis events, and to ensure a timely transfer of the HPCS and RCIC pump suctions to the suppression pool during a SBO. | |||
=====Analysis:===== | =====Analysis:===== | ||
The team determined that the failure to evaluate the capability to transfer HPCS and RCIC pumps suctions from the CST to the suppression pool under cold weather conditions was contrary to 10 CFR Part 50, Appendix B, Criterion III, "Design Control," and 10 CFR 50.63, "Loss of All Alternating Current Power," and was a performance deficiency. The performance deficiency was determined to be more-than-minor because it was associated with the Mitigating Systems cornerstone attribute of design control and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the failure of the HPCS and or RCIC pumps to automatically transfer their suction source from the CST to the suppression pool upon reaching a low CST water level condition could damage the pump(s) thus preventing them to be used to mitigate a transient or accident. | The team determined that the failure to evaluate the capability to transfer HPCS and RCIC pumps suctions from the CST to the suppression pool under cold weather conditions was contrary to 10 CFR Part 50, Appendix B, Criterion III, "Design Control," and 10 CFR 50.63, "Loss of All Alternating Current Power," and was a performance deficiency. The performance deficiency was determined to be more-than-minor because it was associated with the Mitigating Systems cornerstone attribute of design control and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the failure of the HPCS and or RCIC pumps to automatically transfer their suction source from the CST to the suppression pool upon reaching a low CST water level condition could damage the pump(s) thus preventing them to be used to mitigate a transient or accident. | ||
The team determined the finding could be evaluated using the Significance Determination Process (SDP) in accordance with Inspection Manual Chapter (IMC) 0609, "Significance Determination Process," Attachment 0609.04, "Initial Characterization of Findings," issued on October 7, 2016. Because the finding impacted the Mitigating Systems cornerstone, the inspectors screened the finding through IMC 0609 Appendix A, "The Significance Determination Process for Findings At-Power," issued on June 19, 2012, using Exhibit 2, "Mitigating Systems Screening Questions." The team determined the finding required a detailed risk evaluation because the available information provided by the licensee as of September 15, 2017, did not demonstrate reasonable assurance that the HPCS and RCIC pumps would have remained functional with cold weather. Specifically, the team determined that the expected time to freeze the instrument lines was less than the time to reach the CST low level setpoint associated with the pumps suction transfer. . The Senior Reactor Analyst (SRA) performed a detailed risk evaluation using a version of the Perry SPAR Model, Revision 8.19, which had recently been modified with some additional plant specific features that are documented in Inspection Report 05000440/ 2017009. The SRA requested that Idaho National Laboratory slightly modify this revision of the SPAR model to include a basic event modeling the potential for operator action to perform the suction transfer of the HPCS and RCIC systems from the CST to suppression pool if it failed to occur. In the base model, the newly added operator action failure probability was set to 2E-2. This human error probability was estimated using the SPAR Human Reliability Analysis Method for the baseline risk by assuming that the operator failure would be dominated by diagnosis errors and that the only performance driver was a performance shaping factor of High Stress. For this human error probability evaluation, all alarms, instruments, etc. are assumed to function normally and are not affected by the freezing condition. For the degraded condition, the instrument freezing may both prevent the automatic transfer and hinder operator diagnosis of the condition by indicating a false high level in the CST when level is actually decreasing. | The team determined the finding could be evaluated using the Significance Determination Process (SDP) in accordance with Inspection Manual Chapter (IMC) 0609, "Significance Determination Process," Attachment 0609.04, "Initial Characterization of Findings," issued on October 7, 2016. Because the finding impacted the Mitigating Systems cornerstone, the inspectors screened the finding through IMC 0609 Appendix A, "The Significance Determination Process for Findings At | ||
-Power," issued on June 19, 2012, using Exhibit 2, "Mitigating Systems Screening Questions." The team determined the finding required a detailed risk evaluation because the available information provided by the licensee as of September 15, 2017, did not demonstrate reasonable assurance that the HPCS and RCIC pumps would have remained functional with cold weather. Specifically, the team determined that the expected time to freeze the instrument lines was less than the time to reach the CST low level setpoint associated with the pumps suction transfer. . | |||
The Senior Reactor Analyst (SRA) performed a detailed risk evaluation using a version of the Perry SPAR Model, Revision 8.19, which had recently been modified with some additional plant specific features that are documented in Inspection Report 05000440/ | |||
2017009. The SRA requested that Idaho National Laboratory slightly modify this revision of the SPAR model to include a basic event modeling the potential for operator action to perform the suction transfer of the HPCS and RCIC systems from the CST to suppression pool if it failed to occur. In the base model, the newly added operator action failure probability was set to 2E | |||
-2. This human error probability was estimated using the SPAR Human Reliability Analysis Method for the baseline risk by assuming that the operator failure would be dominated by diagnosis errors and that the only performance driver was a performance shaping factor of High Stress. For this human error probability evaluation, all alarms, instruments, etc. are assumed to function normally and are not affected by the freezing condition. For the degraded condition, the instrument freezing may both prevent the automatic transfer and hinder operator diagnosis of the condition by indicating a false high level in the CST when level is actually decreasing. | |||
12 To estimate the change in risk due to the degraded condition, the following assumptions were made: | |||
The degraded condition was modeled as a recoverable failure of the automatic suction transfer function of the HPCS and RCIC systems. | |||
Only the loss of offsite power event trees were evaluated. The level indication and automatic suction swap | |||
-over of the systems remained available for other initiating events. | |||
The CST level instruments and level sensors required for successful suction transfer of HPCS and RCIC from the CST to the suppression pool are not modeled in the SPAR model. The SRA used two existing basic events in the SPAR model as surrogates to represent failure of the automatic suction transfer due to freezing. For the HPCS system, the basic event HCS | |||
-MOV-FT-SUCTR, "HPCS Suction Transfer Fails" was set to "True" or failed. For the RCIC system, the basic event "RCI | |||
-MOV-OO-F010" was also set to "True" or failed. | |||
The basic event for operator action to perform the suction transfer of both systems was evaluated using the SPAR Human Reliability Method. | |||
The SRA assumed the performance shaping factor that would be the most significant performance driver in the degraded condition was ergonomics, as the indication of CST level necessary for diagnosis could be misleading. However, the SRA also determined that operators would be monitoring level, and could determine that the low CST level should have been reached and take the necessary manual action. The ergonomics performance shaping factor was rated as "poor". All other performance shaping factors were set at the nominal values. The resulting human error probability for the failure to perform the suction transfer was 0.2. | |||
The CST is normally maintained with approximately 400,000 gallons of water. The low level CST alarm and automatic suction transfer should normally occur at approximately 98,000 gallons. The RCIC is the preferred system over HPCS for use during LOOP events. Assuming a RCIC flowrate of 700 gpm, many hours of successful operation would occur before any concern with loss of suction | The exposure period was determined to be 58 days. This was based on the past 3 years of weather data reviewed by the licensee to determine, on average, the number of days that the outside temperature was less than 32 degrees Fahrenheit. This is likely a conservative estimate of the exposure period. The UFSAR Table 2.3-3 showed the mean number of days with a high of 32 degrees Fahrenheit as 36 degrees Fahrenheit. The exposure time was further divided into a period of 13 days, which represents the mean time below 17 degrees Fahrenheit, and 45 days, the mean time with a temperature above 17 degrees Fahrenheit but below 32 degrees Fahrenheit. Below 17 degrees Fahrenheit | ||
, plant SBO procedures require using the HPCS system to transfer water from the CST to the suppression pool, which results in a much shorter time to the low CST level and possible pump damage. However, above 17 degrees Fahrenheit, this action is not required, and the time to the low level in the CST would be similar to the LOOP scenarios. | |||
The CST is normally maintained with approximately 400,000 gallons of water. The low level CST alarm and automatic suction transfer should normally occur at approximately 98,000 gallons. The RCIC is the preferred system over HPCS for use during LOOP events. Assuming a RCIC flowrate of 700 gpm, many hours of successful operation would occur before any concern with loss of suction a nd 13 pump trip. This time would allow for the recovery of offsite power and the use of normal inventory control and heat removal systems. To account for the recovery of offsite power and use of normal systems, the SRA multiplied the delta core damage frequency for LOOP scenarios by the appropriate offsite power non-recovery probability at 6 hours. For the portion of the exposure period between 17 degrees Fahrenheit and 32 degrees Fahrenheit (i.e., 45 days), offsite power non | |||
-recovery probabilities were also modified for SBO sequences. No additional recovery of offsite power was credited for LOOP or SBO sequences which also involved one or more stuck open relief valves. | |||
The change core damage frequency from the degraded plant condition was estimated as 7E-7/yr. The dominant sequence involved a SBO event, the failure of the operator to perform the suction transfer resulting in RCIC and HPCS failure, and the failure to recover offsite power. External events were evaluated qualitatively using the risk insights from a previous detailed risk evaluation documented in Inspection Report 05000440/2017009. In that evaluation, the external event risk for LOOP related scenarios was less than the internal event risk, primarily because of a lower external event LOOP frequency obtained from the Individual Plant Examination of External Events. The SRA concluded external event risk would not cause the risk of the finding to exceed the 1E | |||
-6/yr. threshold for a more significant finding. The SRA evaluated LERF by applying a 0.2 LERF factor specified by IMC 0609 Appendix H, "Containment Integrity Significance Determination Process," for plants with a Mark III containment to sequences that represent core damage at high pressure. The delta LERF estimate was determined to be less than 1E | |||
-7/yr. Based on the results of the detailed risk evaluation, the finding was determined to be of very | |||
-low safety significance (Green). | |||
The team did not identify a cross | |||
-cutting aspect associated with this finding because it was not confirmed to reflect current performance due to the age of the performance deficiency. Specifically, the CST instrument lines were designed and the SBO coping strategy during cold weather was established more than 3 years ago. | |||
=====Enforcement:===== | =====Enforcement:===== | ||
Title 10 CFR Part 50, Appendix B, Criterion III, "Design Control," states, in part, that measures shall be established for verifying or checking the adequacy of design, such as by the performance of design reviews, by the use of alternate or simplified calculational methods, or by the performance of a suitable testing program. As of August 23, 2017, the licensee failed to verify the adequacy of design. Specifically, the licensee did not verify the adequacy of the CST low level instruments lines to detect low water level and cause an automatic HPCS and RCIC suction transfer to the suppression pool when the CST supply becomes exhausted during cold weather conditions. The heat tracing of these lines would not provide freeze protection during a 14 LOOP with cold weather and monitoring of the heat tracing was inadequate to detect a failure before the instrument lines estimated freeze time during normal operations with cold weather. In addition, 10 CFR 50.63, "Loss of All Alternating Current Power," requires, in part, that the licensee determine the capability for coping with an SBO of a specified duration by an appropriate coping analysis. Revision 12 of Section 15H, "Station Blackout," of the UFSAR, states "The Perry specific SBO assessment which conforms to 10 CFR 50.63 and Regulatory Guide 1.155 follows." Regulatory Guide 1.155, "Station Blackout," Section 3.2, "Evaluation of Plant-Specific Station Blackout Capability," stated "The following considerations should be included when determining the plant's capability to cope with a station blackout- The design adequacy and capability of equipment needed to cope with a station blackout for the required duration and recovery period should be addressed and evaluated as appropriate for the associated environmental conditions." | Title 10 CFR Part 50, Appendix B, Criterion III, "Design Control," states, in part, that measures shall be established for verifying or checking the adequacy of design, such as by the performance of design reviews, by the use of alternate or simplified calculational methods, or by the performance of a suitable testing program. | ||
As of August 23, 2017, the licensee failed to verify the adequacy of design. Specifically, the licensee did not verify the adequacy of the CST low level instruments lines to detect low water level and cause an automatic HPCS and RCIC suction transfer to the suppression pool when the CST supply becomes exhausted during cold weather conditions. The heat tracing of these lines would not provide freeze protection during a 14 LOOP with cold weather and monitoring of the heat tracing was inadequate to detect a failure before the instrument lines estimated freeze time during normal operations with cold weather. | |||
In addition, 10 CFR 50.63, "Loss of All Alternating Current Power," requires, in part, that the licensee determine the capability for coping with an SBO of a specified duration by an appropriate coping analysis. Revision 12 of Section 15H, "Station Blackout | |||
," of the UFSAR, states "The Perry specific SBO assessment which conforms to 10 CFR 50.63 and Regulatory Guide 1.155 follows." Regulatory Guide 1.155, "Station Blackout," Section 3.2, "Evaluation of Plant | |||
-Specific Station Blackout Capability," stated "The following considerations should be included when determining the plant's capability to cope with a station blackout- The design adequacy and capability of equipment needed to cope with a station blackout for the required duration and recovery period should be addressed and evaluated as appropriate for the associated environmental conditions." | |||
It also stated | |||
, "This should include consideration as appropriate of the following- Potential effects of other hazards, such as weather, on station blackout response equipment-" | |||
As of August 31, 2017, the licensee failed to determine the capability for coping with an SBO by an appropriate coping analysis. Specifically, the coping analysis for an SBO with cold weather incorrectly evaluated the capability to transfer the HPCS suction from the CST to the suppression pool because the licensee underestimated the times to (1) freeze the CST low level instrument lines and (2) transfer the entire CST usable volume and the pump suction to the suppression pool. | |||
The licensee has taken corrective actions to address the finding by monitoring the CST level line heat trace circuits more frequently during normal cold weather operating conditions, updating procedures to alert operators that a loss of power to distribution panel F1A04 will result in a loss of CST level line heat tracing, and to ensure that the HPCS and RCIC suction sources are transferred to the suppression pool before the level lines become non | |||
-functional during cold weather design basis and SBO conditions. | |||
Because this violation was of very | |||
-low safety significance (Green) and was entered into the licensee's CAP as CR | |||
-2017-08685, CR | |||
-2017-08930, and CR | |||
-2017-9006 these violations are being treated as an NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy. (NCV 05000440/2017008 | |||
-01; Failure to Address the Susceptibility of the C ondensate Storage Tank Low Level Instrument Lines to Freeze) | |||
===.4 Mitigating System Modifications=== | ===.4 Mitigating System Modifications=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The team reviewed four permanent plant modifications. This review included in-plant walkdowns for accessible portions of the modified structures, systems, and components. The team reviewed the modifications to verify that the design bases, licensing bases, 15 and performance capability of the components had not been degraded through modifications. The modifications were selected based upon risk significance, safety significance, and complexity. The team reviewed the modifications selected to determine if: | The team reviewed four permanent plant modifications. This review included in | ||
-plant walkdowns for accessible portions of the modified structures, systems, and components | |||
. The team reviewed the modifications to verify that the design bases, licensing bases, 15 and performance capability of the components had not been degraded through modifications. The modifications were selected based upon risk significance, safety significance, and complexity. The team reviewed the modifications selected to determine if: | |||
the supporting design and licensing basis documentation was updated; the changes were in accordance with the specified design requirements; the procedures and training plans affected by the modification have been adequately updated; the test documentation as required by the applicable test programs has been updated; and post-modification testing adequately verified system operability and/or functionality. The team also used applicable industry standards to evaluate acceptability of the modifications. The modifications listed below were reviewed as part of this inspection effort: Addenda A-01 and A-02 to Revision 9 of Calculation 0P42 | |||
-0111, "Self-Weight Excitation Review of Hangers for Emergency Closed Cooling System; | |||
" Engineering Change Package (ECP) 14-0228-001, "New EDG Fuel Oil Level Instruments;" | |||
ECP 09-0573, "Emergency Service Water 'C' Pump Refurbishment;" and ECP 11-0755, "Place Sand Bags in Control Complex at Door IB | |||
-103." | |||
====b. Findings==== | ====b. Findings==== | ||
Line 103: | Line 267: | ||
=====Introduction:===== | =====Introduction:===== | ||
The team identified a finding of very-low safety significance (Green) and an associated NCV of 10 CFR Part 50, Appendix B, Criterion III, "Design Control," for the failure to consider all stresses resulting from the as built pipe support connection details. Specifically, the evaluation for pipe support 1P42-H1080 did not address the impact of rigid connections at both ends of the W8 steel post and of the lateral load on W21 auxiliary steel beam. | The team identified a finding of very | ||
-low safety significance (Green) and an associated NCV of 10 CFR Part 50, Appendix B, Criterion III, "Design Control," for the failure to consider all stresses resulting from the as built pipe support connection details. Specifically, the evaluation for pipe support 1P42 | |||
-H1080 did not address the impact of rigid connections at both ends of the W8 steel post and of the lateral load on W21 auxiliary steel beam. | |||
=====Description:===== | =====Description:===== | ||
In 1985, the licensee evaluated the safety-related emergency closed cooling system pipe support 1P42-H1080 in Calculation 0P42-0111, Revision 9. The calculation was revised through addenda A-01 and A-02, on September 4, 2014, and September 25, 2015, respectively, to evaluate the addition of conduits associated with the spent fuel pool instrumentation modification. During this inspection, the team noted that the pipe support configuration consisted of a vertical W31 steel post installed at elevation 620 feet in the intermediate building with the top end rigidly attached to the bottom of the floor at the 654 foot elevation. Thus, in case of any differential vertical displacements between the two floors due to change in live 16 loads or under a seismic event, this configuration would result in a significant transfer of the floor loading to the post. However, Calculation 0P42-0111, including its addenda A-01 and A-02, did not address this configuration. Specifically, it failed to account for the additional loads associated with the relative displacements of the floors. The licensee captured this concern in their CAP as CR-2017-08986 on August 30, 2017. In addition, the team noted that the post was laterally supported at about mid-height through a brace to a W21 beam originally installed as an auxiliary steel member to support cable trays. Calculation 0P42-0111 concluded that the associated stresses in W21 beam would be small and acceptable based on judgment. However, the licensee did not document a basis supporting this judgement and a preliminary review by the team and the licensee during this inspection period determined that the stresses could be significant enough to necessitate more detailed analysis. The licensee captured this concern in their CAP as CR-2017-09043 on August 31, 2017. The licensee's immediate corrective actions included an evaluation that reasonably concluded that after consideration of the relative displacements between the floors and with more refined evaluations, the stresses in the pipe support members and the W21 steel beam will remain within the operability limits. The proposed corrective actions to restore compliance at the time of this inspection was to re-evaluate the structural analyses. | In 1985, the licensee evaluated the safety | ||
-related emergency closed cooling system pipe support 1P42 | |||
-H1080 in Calculation 0P42 | |||
-0111, Revision 9. The calculation was revised through addenda A | |||
-01 and A-02, on September 4, 2014, and September 25, 2015, respectively, to evaluate the addition of conduits associated with the spent fuel pool instrumentation modification. | |||
During this inspection, the team noted that the pipe support configuration consisted of a vertical W31 steel post installed at elevation 620 feet in the intermediate building with the top end rigidly attached to the bottom of the floor at the 654 foot elevation. Thus, in case of any differential vertical displacements between the two floors due to change in live 16 loads or under a seismic event, this configuration would result in a significant transfer of the floor loading to the post. However, Calculation 0P42 | |||
-0111, including its addenda A-01 and A-02, did not address this configuration. Specifically, it failed to account for the additional loads associated with the relative displacements of the floors. | |||
The licensee captured this concern in their CAP as CR | |||
-2017-08986 on August 30, 2017. | |||
In addition, the team noted that the post was laterally supported at about mid | |||
-height through a brace to a W21 beam originally installed as an auxiliary steel member to support cable trays. Calculation 0P42 | |||
-0111 concluded that the associated stresses in W21 beam would be small and acceptable based on judgment. However, the licensee did not document a basis supporting this judgement and a preliminary review by the team and the licensee during this inspection period determined that the stresses could be significant enough to necessitate more detailed analysis. The licensee captured this concern in their CAP as CR | |||
-2017-09043 on August 31, 2017. | |||
The licensee's immediate corrective actions included an evaluation that reasonably concluded that after consideration of the relative displacements between the floors and with more refined evaluations, the stresses in the pipe support members and the W21 steel beam will remain within the operability limits. The proposed corrective actions to restore compliance at the time of this inspection was to re | |||
-evaluate the structural analyses. | |||
=====Analysis:===== | =====Analysis:===== | ||
The team determined the failure to consider all stresses resulting from the as built pipe support connection was contrary to 10 CFR Part 50, Appendix B, Criterion III, "Design Control," and was a performance deficiency. The performance deficiency was determined to be more-than-minor because it was associated with the Mitigating Systems cornerstone attribute of design control and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the failure to analyze actual pipe configuration and to evaluate the W21 beam did not ensure the emergency closed cooling system and its safety-related supported loads would remain available and capable of providing their accident mitigating function | The team determined the failure to consider all stresses resulting from the as built pipe support connection was contrary to 10 CFR Part 50, Appendix B, Criterion III, "Design Control," and was a performance deficiency. The performance deficiency was determined to be more | ||
-than-minor because it was associated with the Mitigating Systems cornerstone attribute of design control and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the failure to analyze actual pipe configuration and to evaluate the W21 beam did not ensure the emergency closed cooling system and its safety-related supported loads would remain available and capable of providing their accident mitigating function. | |||
17 The team determined that this finding had a cross-cutting aspect in the area of human performance because the licensee did not recognize and plan for the possibility of mistakes, latent issues, and inherent risk, even while expecting successful outcomes. Specifically, the licensee did not recognize this latent issue when revising the structural evaluation in 2015. [H.12] | The team determined the finding could be evaluated using the SDP in accordance with IMC 0609, "Significance Determination Process," Attachment 0609.04, "Initial Characterization of Findings," issued on October 7, 2016. Because the finding impacted the Mitigating Systems cornerstone, the inspectors screened the finding through IMC 0609 Appendix A, "The Significance Determination Process for Findings At | ||
-Power," issued on June 19, 2012, using Exhibit 2, "Mitigating Systems Screening Questions." | |||
The finding screened as of very | |||
-low safety significance (Green) because it did not result in the loss of operability or functionality of mitigating systems. Specifically, the licensee performed an operability determination which concluded that the differential movements between the floors would be very small and that the resulting stresses would reasonably be bounded by the applicable stress operability limits. Licensee evaluation also indicated that the W21 beam stresses would meet the applicable operability limits. | |||
17 The team determined that this finding had a cross | |||
-cutting aspect in the area of human performance because the licensee did not recognize and plan for the possibility of mistakes, latent issues, and inherent risk, even while expecting successful outcomes. Specifically, the licensee did not recognize this latent issue when revising the structural evaluation in 2015. | |||
[H.12] | |||
=====Enforcement:===== | =====Enforcement:===== | ||
Title 10 CFR Part 50, Appendix B, Criterion III, "Design Control," states, in part, that measures shall be established for verifying or checking the adequacy of design, such as by the performance of design reviews, by the use of alternate or simplified calculational methods, or by the performance of a suitable testing program. Contrary to the above, since August 7, 1985, the licensee failed to verify the adequacy of the design. Specifically, the licensee did not verify the design adequacy of support 1P42-H1080 because the associated structural evaluation failed to consider the impact of the rigid end connections of the W8 steel post and also failed to demonstrate acceptability of the W21 beam affected by the pipe support. The licensee is still evaluating its planned corrective actions. However, the team determined that the continued non-compliance does not present an immediate safety concern because the licensee performed an evaluation that reasonably concluded that the affected structures will remained operable. Because this violation was of very-low safety significance (Green) and was entered into the licensee's CAP as CR-2017-08986 and CR-2017-09043, this violation is being treated as an NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy. (NCV 05000440/2017008-02; Inadequate Evaluation of Emergency Closed Cooling System Pipe Support). | Title 10 CFR Part 50, Appendix B, Criterion III, "Design Control," states, in part, that measures shall be established for verifying or checking the adequacy of design, such as by the performance of design reviews, by the use of alternate or simplified calculational methods, or by the performance of a suitable testing program. | ||
Contrary to the above, since August 7, 1985, the licensee failed to verify the adequacy of the design. Specifically, the licensee did not verify the design adequacy of support 1P42-H1080 because the associated structural evaluation failed to consider the impact of the rigid end connections of the W8 steel post and also failed to demonstrate acceptability of the W21 beam affected by the pipe support. | |||
The licensee is still evaluating its planned corrective actions. However, the team determined that the continued non | |||
-compliance does not present an immediate safety concern because the licensee performed an evaluation that reasonably concluded that the affected structures will remained operable | |||
. Because this violation was of very | |||
-low safety significance (Green) and was entered into the licensee's CAP as CR | |||
-2017-08986 and CR | |||
-2017-09043, this violation is being treated as an NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy. (NCV 05000440/2017008 | |||
-02; Inadequate Evaluation of Emergency Closed Cooling System Pipe Support) | |||
. | |||
===.5 Operating Experience=== | ===.5 Operating Experience=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The team reviewed three operating experience issues (samples) to ensure that generic concerns had been adequately evaluated and addressed by the licensee. The operating experience issues listed below were reviewed as part of this inspection: | The team reviewed three operating experience issues (samples) to ensure that generic concerns had been adequately evaluated and addressed by the licensee. The operating experience issues listed below were reviewed as part of this inspection: | ||
IN 2007-01, "Recent Operating Experience Concerning Hydrostatic Barriers;" | |||
IN 2015-01, "Degraded Ability To Mitigate Flooding Events;" | |||
and Part 21 No. 2013 00, "Wedge Pin Failure of an Anchor/Darling Double | |||
-Disc Gate Valve at Browns Ferry Nuclear Plant U1." | |||
====b. Findings==== | ====b. Findings==== | ||
Line 129: | Line 338: | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The team performed a detailed reviewed of the procedures listed below. The procedures were compared to UFSAR, design assumptions, and training materials to assess their consistency. The following operating procedures were reviewed in detail: | The team performed a detailed reviewed of the procedures listed below. The procedures were compared to UFSAR, design assumptions, and training materials to assess their consistency | ||
. The following operating procedures were reviewed in detail: | |||
Emergency Operating Procedure (EOP)-01A Chart, "Level Power Control," Revision H; EOP-02 Chart, "Primary Containment Control," Revision F; EOP-SPI 3.2, "Suppression Pool Makeup," Revision 1; EOP-SPI 6.4, "HPCS Injection," Revision 2; EOP-SPI 6.6, "RCIC Injection and Pressure Control," Revision 3; ONI-R10-1, "Loss of AC Power," Revision A; ONI-R10-2, "Station Blackout," Revision B; ONI-SPI C-3, "CST Transfer to Suppression Pool," Revision 4; ONI-SPI C-7, "Division 3 to Division 2 480 Volt Crosstie," Revision 5; ONI-SPI D-1, "Maintaining System Availability," Revision 5; ONI-SPI D-3, "Cross Tie Unit Batteries," Revision 5; ONI-ZZZ-1, "Tornado or High Winds," Revision 28; SOI-P45/P49, "Emergency Service Water and Screen Wash Systems," Revision 30; and SOI-P57, "Safety Related Instrument Air System," Revision 17. For the procedures listed, time dependent operator actions were reviewed for reasonableness. This review included walk downs of in | |||
-plant actions with a licensed operator and the observations of licensed operator crews actions during the performance o f an SBO scenario in the station's simulator to assess operator knowledge level, adequacy of procedures, and availability of special equipment where required, and capability to perform time dependent operator actions within the required time. In addition, the team evaluated operations interfaces with other departments. The following operator actions were reviewed: | |||
Emergency Service Water Pump Strainer(s) Manual Backwash during a LOOP | |||
; Supply Outboard Main Steam Isolation Valve following a Loss of Instrument Air; Break Vacuum in the Emergency Service Water System during Internal Flooding; Restore Emergency AC Power following SBO recovery; Swap CST Suction from the CST to the Suppression Pool during a Tornado Warning; Operations of HPCS and RCIC during in EOP | |||
-1 during Cold Weather Conditions; Transfer CST Water to Suppression Pool Directly during Cold Weather SBO; Dump the Upper Containment Pool into the Suppression Pool during an SBO; Power Containment Isolation Valves during an SBO; Cross-tie Unit Batteries during an SBO; Cross-tie Division II to Division III during an SBO; and Open Control Room Cabinets during an SBO. | |||
====b. Findings==== | ====b. Findings==== | ||
Line 135: | Line 350: | ||
=====Introduction:===== | =====Introduction:===== | ||
The team identified a finding of very-low safety significance (Green) and an associated NCV of 10 CFR Part 50, Appendix B, Criterion III, "Design Control," for the failure to verify the capability to manually backwash the Emergency Service Water (ESW) strainer during a LOOP. Specifically, the licensee credited the capability to manually backwash the ESW strainers during a LOOP. However, the associated differential pressure alarm setpoint did not ensure sufficient time to complete this activity because the alarms were set at the same value as the design differential pressure value assumed by the hydraulic calculations. | The team identified a finding of very | ||
-low safety significance (Green) and an associated NCV of 10 CFR Part 50, Appendix B, Criterion III, "Design Control," for the failure to verify the capability to manually backwash the Emergency Service Water (ESW) strainer during a LOOP. Specifically, the licensee credited the capability to manually backwash the ESW strainers during a LOOP. However, the associated differential pressure alarm setpoint did not ensure sufficient time to complete this activity because the alarms were set at the same value as the design differential pressure value assumed by the hydraulic calculations. | |||
Description | |||
: The ESW system is equipped with strainers that need to be manually backwashed during a LOOP with high differential pressure. Specifically, Revision 12 of UFSAR Section 9.2.1, "Emergency Service Water System," stated | |||
, "The emergency service water strainers are driven by nonsafety | |||
-related motors from nonsafety | |||
-related power supplies." In addition, it stated | |||
, "Manual backwash will, therefore, be required after a LOOP. | |||
" Plant procedure s direct operators to manually backwash the strainers if a high differential pressure alarm is received. | |||
However, the team noted that the high differential pressure alarm setpoint value did not provide sufficient time to complete the manual backwash before clogging conditions adversely affect the ESW system flow. Specifically, the licensee estimated that it would take approximately 2 to 3 hours to manually backwash the strainers during an in | |||
-field walk down of the backwash procedure that the team observed. In contrast, ESW Hydraulic Calculation P45 | |||
-057, "Emergency Service Water System Thermal Hydraulic Model," Revision 3, assumed a strainer differential pressure value that was equal to the alarm setpoint. Thus, the alarm setpoint did include any allowance for additional debris accumulation on the strainer while the manual backwash is completed. | |||
The licensee captured the team's concerns in their CAP as CR | |||
-2017-09033 on August 31, 2017. The immediate corrective action was to perform a past and current operability review that reasonably determined the ESW remained operable by crediting unused margin reserved for potential pump degradation. The proposed corrective actions to restore compliance was to revise the associated calculation and the alarm setpoint to ensure sufficient to perform the required manual actions during a LOOP. | |||
=====Analysis:===== | =====Analysis:===== | ||
The team determined that the failure to verify the capability to manually backwash the ESW strainer during LOOP was contrary to 10 CFR Part 50, Appendix B, Criterion III, "Design Control," and was a performance deficiency. The performance 20 deficiency was determined to be more-than-minor because it was associated with the Mitigating Systems cornerstone attribute of protection against external factors and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the performance deficiency did not assure the ESW capability to supply the required minimum flow to its supported components. The team determined the finding could be evaluated using the SDP in accordance with IMC 0609, "Significance Determination Process," Attachment 0609.04, "Initial Characterization of Findings," issued on October 7, 2016. Because the finding impacted the Mitigating Systems cornerstone, the team screened the finding through IMC 0609, Appendix A, "The Significance Determination Process for Findings At-Power," issued on June 19, 2012, using Exhibit 2, "Mitigating Systems Screening Questions." The finding screened as of very-low safety significance (Green) because it did not result in the loss of operability or functionality of mitigating systems. Specifically, the licensee performed a past and current operability review that reasonably determined the ESW remained operable by crediting unused margin reserved for potential pump degradation. The team did not identify a cross-cutting aspect associated with this finding because it was not confirmed to reflect current performance due to the age of the performance deficiency. Specifically, the alarm setpoint was established more than 3 years ago. | The team determined that the failure to verify the capability to manually backwash the ESW strainer during LOOP was contrary to 10 CFR Part 50, Appendix B, Criterion III, "Design Control," and was a performance deficiency. | ||
The performance 20 deficiency was determined to be more | |||
-than-minor because it was associated with the Mitigating Systems cornerstone attribute of protection against external factors and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the performance deficiency did not assure the ESW capability to supply the required minimum flow to its supported components. | |||
The team determined the finding could be evaluated using the SDP in accordance with IMC 0609, "Significance Determination Process," Attachment 0609.04, "Initial Characterization of Findings," issued on October 7, 2016. Because the finding impacted the Mitigating Systems cornerstone, the team screened the finding through IMC 0609, Appendix A, "The Significance Determination Process for Findings At-Power," issued on June 19, 2012, using Exhibit 2, "Mitigating Systems Screening Questions." The finding screened as of very | |||
-low safety significance (Green) because it did not result in the loss of operability or functionality of mitigating systems. Specifically, the licensee performed a past and current operability review that reasonably determined the ESW remained operable by crediting unused margin reserved for potential pump degradation. | |||
The team did not identify a cross | |||
-cutting aspect associated with this finding because it was not confirmed to reflect current performance due to the age of the performance deficiency. | |||
Specifically, the alarm setpoint was established more than 3 years ago. | |||
Enforcement | |||
: Title 10 CFR Part 50, Appendix B, Criterion I II, "Design Control," states, in part, that measures shall be established for verifying or checking the adequacy of design, such as by the performance of design reviews, by the use of alternate or simplified calculational methods, or by the performance of a suitable testing program. | |||
Contrary to the above, as of August 31, 2017, the licensee failed to verify the design adequacy of ESW, a safety | |||
-related system | |||
. Specifically, the licensing basis credited the capability to manually backwash the ESW strainers during a LOOP. However, the associated differential pressure alarm setpoint did not ensure sufficient time to complete this activity because the alarms were set at the same value as the design differential pressure value assumed by the hydraulic calculations. The licensee is still evaluating its planned corrective actions. However, this issue does not present an immediate safety concern because the licensee performed a past and current operability review that reasonably determined the ESW had unused margin reserved for pump degradation that could be temporarily used to allow sufficient time to complete a manual backwash during a LOOP | |||
. Because this violation was of very | |||
-low safety significance (Green) and was entered into the licensee's CAP as CR | |||
-2017-09033, this violation is being treated as an NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy. | |||
(NCV 05000440/2017008 | |||
-03, Failure to Verify the Capability to Manually Backwash the Emergency Service Water Strainer during Loss of Offsite Power | |||
) | |||
==OTHER ACTIVITIES== | ==OTHER ACTIVITIES== | ||
Line 150: | Line 401: | ||
==4OA2 Identification and Resolution of Problems== | ==4OA2 Identification and Resolution of Problems== | ||
===.1 Review of Items Entered Into the Corrective Action Program | ===.1 Review of=== | ||
Items Entered Into the Corrective Action Program | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The team reviewed a sample of problems identified by the licensee associated with the selected samples and that were entered into the CAP. The team reviewed these issues to verify an appropriate threshold for identifying issues and to evaluate the effectiveness of corrective actions related to design issues. In addition, corrective action documents written on issues identified during the inspection were reviewed to verify adequate problem identification and incorporation of the problem into the CAP. The specific corrective action documents sampled and reviewed by the team are listed in the attachment to this report. The team also selected four issues identified during previous component design basis inspections to verify that the | The team reviewed a sample of problems identified by the licensee associated with the selected samples and that were entered into the CAP. The team reviewed these issues to verify an appropriate threshold for identifying issues and to evaluate the effectiveness of corrective actions related to design issues. In addition, corrective action documents written on issues identified during the inspection were reviewed to verify adequate problem identification and incorporation of the problem into the CAP. The specific corrective action documents sampled and reviewed by the team are listed in the attachment to this report. | ||
The team also selected four issues identified during previous component design basis inspections to verify that the concern s were adequately evaluated and corrective actions were identified and implemented to resolve the concern, as necessary. The following issues were reviewed: | |||
NCV 05000440/2006009 | |||
-04, "Inadequate Procedures for Controlling Flow into Reactor Vessel;" | |||
NCV 05000440/2011008 | |||
-01, "Failure to Adequately Protect Safety | |||
-Related Equipment from Internal Flooding;" | |||
NCV 05000440/2011008 | |||
-02, "Inadequate Control Circuit Voltage Calculation for Safety-Related Contactors;" and NCV 05000440/2016007 | |||
-02, "Use of Unapproved Standard for Site Flooding Modification and Associated | |||
=====Analysis.===== | =====Analysis.===== | ||
Line 159: | Line 422: | ||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified | ||
. | |||
{{a|4OA6}} | {{a|4OA6}} | ||
==4OA6 Management Meetings== | ==4OA6 Management Meetings== | ||
===.1 Interim Meeting Summary On September | ===.1 Interim Meeting Summary=== | ||
The licensee acknowledged the issues presented. The team confirmed that several documents reviewed were considered proprietary and were handled in accordance with the NRC policy related to proprietary information. The team had outstanding questions that required additional review and a follow-up exit meeting. | |||
On September 1 4, 2017, the team presented the preliminary inspection results to Mr. D. Hamilton and other members of the licensee staff. The licensee acknowledged the issues presented. The team confirmed that several documents reviewed were considered proprietary and were handled in accordance with the NRC policy related to proprietary information. The team had outstanding questions that required additional review and a follow | |||
-up exit meeting. | |||
22 | 22 | ||
===.2 Exit Meeting Summary On November 22, 2017, the team presented the inspection results to Mr. N. Conicella and other members of the licensee staff. | ===.2 Exit Meeting Summary=== | ||
The licensee acknowledged the issues presented. | |||
On November 22, 2017, the team presented the inspection results to Mr. N. Conicella and other members of the licensee staff. The licensee acknowledged the issues presented. | |||
The team asked the licensee whether any materials examined during the inspection should be considered proprietary. Several documents reviewed by the team were considered proprietary information and were either returned to the licensee or handled in accordance with NRC policy on proprietary information. | |||
ATTACHMENT: | |||
: | |||
== | =SUPPLEMENTAL INFORMATION= | ||
SUPPLEMENTAL INFORMATION KEY POINTS OF CONTAC | |||
T Licensee | |||
: | : [[contact::D. Hamilton]], Vice President | ||
: | : [[contact::F. Payne]], Plant General Manager | ||
: | : [[contact::N. Conicella]], Regulatory Compliance Manager | ||
: | : [[contact::D. Reeves]], Site Engineering Director | ||
: [[contact::L. Zerr]], Regulatory Compliance Supervisor | |||
: | : [[contact::T. Kledzik]], Regulatory Compliance Engineer | ||
: | U.S. Nuclear Regulatory Commission | ||
M. Jeffers | |||
, Branch Chief | |||
: [[contact::N. Féliz Adorno]], Senior Reactor Inspector | |||
LIST OF ITEMS OPENED, CLOSED, AND DISCUS | |||
SED Opened and Closed | |||
05000440/2017008 | |||
-01 NCV Failure to Address the Susceptibility of the Condensate Storage Tank | |||
Low Level Instrument Lines to Freeze (Section 1R21.3.b(1)) | |||
05000440/2017008 | |||
-02 NCV Inadequate Evaluation of Emergency Closed Cooling System Pipe Support | |||
(Section1R21.4.b(1)) | |||
05000440/2017008 | |||
-03 NCV Failure to Verify the Capability to Manually Backwash the Emergency Service Water | |||
Strainer during Loss of Offsite Power | |||
(Section 1R21.6.b(2)) | |||
Discussed | |||
None | |||
LIST OF DOCUMENTS REVIEWED The following is a list of documents reviewed during the inspection. Inclusion on this list does not imply that the NRC inspectors reviewed the documents in their entirety, but rather, that selected sections of portions of the documents were evaluated as part of the overall | |||
inspection effort. Inclusion of a document on this list does not imply NRC acceptance of the document or any part of it, unless this is stated in the body of the inspection report. | |||
CALCULATIONS | |||
Number Description or Title | |||
Date or Revision PSTG-0001 PNPP Class 1E Power Distribution System Voltage Study | |||
PRMV-0062 4.16 kV Degraded Voltage Instrumentation Loop Calculation | |||
MISC-0017 Effect of Voltage and Frequency on Induction Motors 0 PRMV-0016 High Pressure Core Spray Motor 1E22C001 Protective Relays Setpoints | |||
MISC-0017 Effect of Voltage and Frequency on Induction Motor Speed | |||
PRMV-0008 U1 EH Bus Supply Breakers, Preferred and Alternate | |||
PRMV-0014 Div 3 HPCS Diesel Generator (1E22S001)/EH1301 Protective Relaying Setpoints | |||
SBO-007 A01 Loss of Heat Tracing | |||
- CST/HPCS Instrument Line | |||
E22-043 HPCS System Thermal | |||
-Hydraulic Analysis | |||
0P42-0111 Self-Weight Excitation Review of Hangers for Emergency Closed Cooling System | |||
9, A-02 4:04.9.2 P57 Tank Anchor Bolt Design | |||
EA0021 P57 Low Pressure Storage Tanks | |||
P57-13 Required Air Volume and Leakage Acceptance Criteria for the Division 1 and 2 Safety Related Instrument Air (P57) System | |||
1P57-101-#007 Calculation for Pipe Supports MK | |||
-1P57-H1140 / H1141 | |||
2/05/1984 PRDC-0016 Division 3, 125 Vdc Load Evaluation, Voltage Drop, Battery/Charger Sizing Calculation | |||
PRDC-0017 Hydrogen Gas Generation in Unit 1 & 2 Division 3 Battery Rooms 0 PSTG-0001 MCC Voltages for Control Circuits | |||
PRDC-0002 Unit 1 Divisions 1, 2 and 3 125 Vdc System Coordination | |||
E22-042 Division 3 Emergency Diesel Generator Jacket Water Heat Exchanger Performance Test | |||
P45-T02 Non-Safety Related Setpoint Tolerances for Emergency | |||
Service/ Standby Diesel generators Heat Exchangers Low Flow Alarm 1P45N0073A/B | |||
SBO-007 Loss of Heat Tracing | |||
- CST/HPCS Instrument Line | |||
0, A-01 R45C04 Div 1, 2, & 3 Diesel Generator Fuel Oil Day Tank improved Technical Specification Volume Calculation | |||
CALCULATIONS | |||
Number Description or Title | |||
Date or Revision E22-037 Design Basis Heat Load & Required ESW Flow for the HPCS DGJW HX 2 E22-041 Div 3 Emergency Diesel Generator Jacket Water Heat | |||
Exchanger Performance Test Evaluation 8/27/03 | |||
E22-042 Division 3 Emergency Diesel Generator Jacket Water Heat Exchanger Performance Test | |||
CALCULATIONS | |||
Number Description or Title | |||
: | Revision E22-029 SVI-E22-T2001 , HPCS Pump Performance Test Acceptance Criteria 7 E22-043 High Pressure Core Spray (HPCS) System Thermal | ||
-Hydraulic Analysis | |||
R45-009 Determine Fuel Oil Volume Required to Support Operation of Standby and HPCS Diesel Generators | |||
P45-023 Emergency Service Water (ESW/P45) System Overpressure Analysis 3 R44-007 Starting Air Leakage Criteria for the Standby and HPCS EDGs Starting Air (R44) System | |||
P45-057 ESW System Thermal Hydraulic Model | |||
CORRECTIVE ACTION DOCUMENTS GENERATED DUE TO THE INSPECTION | |||
Number Description or Title | |||
Date CR-2017-08481 NRC ID DBI Inspection: Minor Discrepancy Identified in SRIA Training Material | |||
08/15/2017 CR-2017-08504 NRC ID DBAI Inspection: Calculation Clarification Required | |||
08/16/2017 CR-2017-08685 NRC ID DBAI Inspection: Question Regarding Contingency Actions During Cold Weather and CST Level Instrumentation | |||
08/23/2017 CR-2017-08725 NRC ID DBI Inspection: Use of Unconservative Concrete Compressive Strength in P57 Anchor Bolt Design Calculation | |||
08/23/2017 CR-2017-08767 NRC ID DBAI Inspection: Station Blackout Time Critical Operator Actions 08/24/2017 CR-2017-08918 NRC ID DBAI Inspection: Procedure Inadequacy Related to Having HPCS Aligned to the Suppression Pool during an SBO | |||
08/29/2017 CR-2017-08920 NRC ID DBAI Inspection: ONI | |||
-R10 Improvements needed for SBO Time Critical Operator Actions | |||
08/29/2017 CR-2017-08923 NRC ID DBAI Inspection: NRC Observation Related to EDG Starting Air | |||
08/29/2017 | |||
CORRECTIVE ACTION DOCUMENTS GENERATED DUE TO THE INSPECTION | |||
Number Description or Title | |||
Date CR-2017-08481 NRC ID DBI Inspection: Minor Discrepancy Identified in SRIA Training Material | |||
08/15/2017 CR-2017-08504 NRC ID DBAI Inspection: Calculation Clarification Required | |||
08/16/2017 CR-2017-08685 NRC ID DBAI Inspection: Question Regarding Contingency Actions During Cold Weather and CST Level Instrumentation | |||
08/23/2017 CR-2017-08725 NRC ID DBI Inspection: Use of Unconservative Concrete Compressive Strength in P57 Anchor Bolt Design Calculation | |||
08/23/2017 CR-2017-08930 NRC ID DBAI Inspection: Calculation SBO | |||
-007 Conservatism and Degraded CST Instrumentation Line Insulation | |||
08/29/2017 CR-2017-08981 NRC ID DBAI Inspection: Minimum Temperature Not Included in HX Test Instruction | |||
08/30/2017 CR-2017-08986 NRC ID DBAI Inspection: Emergency Closed Cooling Pipe Support 1P42H1080 Calculation (0P42 | |||
-0111 Rev. 9, A | |||
-02) Inadequacies | |||
08/30/2017 CR-2017-08967 NRC ID DBAI Inspection: Timed Constrained Operator Actions Validation | |||
08/30/2017 CR-2017-09005 NRC ID DBAI Inspection: HPCS Alignment During a Tornadoes Warning Effects on the SBO Analysis | |||
08/31/2017 CR-2017-09006 NRC ID DBAI Inspection: The SBO Analysis Requires 150k Gallons of Water from the CST which Affects ONI | |||
-R10 Requirements | |||
08/31/2017 CR-2017-09033 NRC ID DBAI Inspection: ESW Discharge Strainer Differential Pressure Alarms are Equivalent to the Design Maximum Value | |||
08/31/2017 CR-2017-09036 NRC ID DBAI Inspection: Minor Error in Calculation 4:04.09.002 | |||
08/31/2017 CR-2017-09043 NRC ID DBI Inspection: Inadequate Justification Provided in Calculation 0P42 | |||
-0111 A-02 Regarding Impact on the Attached Beam 08/31/2017 CORRECTIVE ACTION DOCUMENTS REVIEWED DURING THE INSPECTION | |||
Number Description or Title | |||
Date CR-2013-11377 NRC ID 2013 50.59: LTA 50.59 Evaluation 09 | |||
-01526 07/24/2013 CR-2013-11217 NRC ID 50.59 2013 | |||
- Deficiencies with 50.59 Evaluation | |||
09-01526 07/22/2013 CR-2013-10798 NRC ID 50.59, LTA Controls and Evaluation for SVI | |||
-G33-T9131 for Irradiated Fuel in Upper Pool Storage Rack | |||
07/15/2013 CR-2013-03364 High Pressure Core Spray (HPCS) Pump Performance | |||
03/07/2013 CR-2014-11711 Snapshot Self | |||
-Assessment SN | |||
-SA-2014-0498 - Perry HPCS Pump & Motor ECP Readiness | |||
07/14/2014 CR-2012-12844 EMI Test Results Indicate Increase Emissions 08/12/2012 CR-2013-03461 10 CFR Part 21 Issued for Components Applicable to Perry | |||
03/08/2013 CR-2013-06927 Transmittal of BWROG TP | |||
-13-006 05/02/2013 | |||
CORRECTIVE ACTION DOCUMENTS REVIEWED DURING THE INSPECTION | |||
Number Description or Title | |||
Date CR-2017-06730 Updated Industry Guidance to Address Part 21 Issue with Anchor Darling Double Disc Gate Valves | |||
06/20/2017 CR-2015-08036 PFA Needed for Site Flooding Issues | |||
06/08/2015 CR-2015-0579 External Flooding during a Probable Maximum Flooding Event | |||
05/12/2015 CR-2016-11864 NRC ID: Underdrain Manhole Covers Changed to Grating vs. Watertight Covers | |||
10/04/2016 CR-2006-00817 NRC ID - CDBI, Affects Drywell Backpressure Not Addressed in Calculation P57 | |||
-13 02/17/2006 CR-2016-26104 Wrong ID Number/Barcode on DLR Label | |||
08/02/2016 CR-2011-06107 CDBI 2011 | |||
- ESW Discharge Valve Uses Modified Acceptance Criteria when Determining Adequate Starting Voltage | |||
11/30/2011 CR-2011-05495 NRC CDBI- PSTG-0030 Omission of Resistive Values | |||
11/15/2011 CR-2011-06244 NRC CDBI 2011 | |||
- Potential Green Non | |||
-Cited Violation | |||
2/02/2011 CR-2012-01195 NRC CDBI NCV, Inadequate Control Circuit | |||
Voltage Calculation for Safety | |||
-Related Motor Starter Contactors | |||
: | 01/24/2012 CR-2011-06226 2011 CDBI | ||
- Potential Green Non | |||
-Cited Violation | |||
2/02/2011 CR-2005-04296 NRC Published IN 05 | |||
-11 05/16/2005 CR-2005-05933 NRC Observation of Building Floor Plugs | |||
08/01/2005 CR-2011-05217 Internal Flooding Calculation Assumptions for system Isolation Not Identified | |||
11/10/2011 CR-2010-87582 Technical Basis for Div 3 Air Rec Inlet Ckv Vlv EC Testing Cannot Be Found | |||
2/29/2010 CR-2015-14494 Excessive Analytical Uncertainty Associated with Test Data Obtained per PTI | |||
-R46-P00001-B 10/23/2015 CR-2012-11858 Degraded Insulation on Piping in the CST Dike for Heat Trace | |||
07/31/2012 CR-2015-02273 CST Level Transmitters Room Temp | |||
- Monitoring Heat Trace Not Maintaining Proper Temperature | |||
2/22/2015 CR-2011-05217 Internal Flooding Calculation Assumptions for System Isolation Not Identified | |||
11/10/2011 CR-2011-06227 Reportability Requirements For Internal Flooding Calculation | |||
JL-083 Issues (NCV) | |||
2/12/2011 CR-2011-06237 Non-Cited Violation for Operator Actions Assumed in JL | |||
-083 Not Translated into Procedures | |||
2/12/2011 CR-2011-06530 8-Hour ENS Report Needed for Control Complex Flooding Calculation Issue | |||
2/07/2011 CR-2012-01194 NRC CDBI NCV, Failure to Adequately Protect Safety Related Equipment from Internal Flooding | |||
01/24/2012 CR-2015-08036 PFA Needed for Site flooding Issues | |||
06/08/2015 CR-2015-14025 10CFR50.59 Review Committee Identified Concerns with 50.59 Eval 14-01234 10/16/2015 | |||
CORRECTIVE ACTION DOCUMENTS REVIEWED DURING THE INSPECTION | |||
Number Description or Title | |||
Date CR-2016-06744 2016 NRC Mod/ 50.59 Inspection: Evaluation 14 | |||
-01234 (PNPP External Flooding) Questions | |||
05/13/2016 CR-2016-06882 2016 NRC Mod/ 50.59 Inspection: 50.59 Evaluation 14 | |||
-01234 Departure in Methodology Required Prior NRC Approval | |||
05/18/2016 CR-2015-05079 External Flooding during a Probable Maximum Flooding Event (West Side of Plant) | |||
04/12/2015 DRAWINGS Number Description or Title | |||
Date or Revision 206-0010-00000-FF Main One Line Diagram 13.8kV & 4.16kV | |||
FF 208-0218- 00006-S Back Up Fuel Oil Transfer Pump 1R45 | |||
-C002C S 206-0015-00000-FF Non Class 1E 13.8kV Start | |||
-Up Bus L10 & L20 | |||
FF D-206-018 One Line Diagram Class 1E 4.16kV Bus EH13 | |||
Z 022-0010-00000 Environmental Conditions for Control Building | |||
K 1190E21 1P57-A003B, SRIA Storage Tank, Sh 1, 2 | |||
MK-1P42-H1080 Pipe Support Drawing | |||
B 215-0431-00501 Conduit Layout, Intermediate Building | |||
- North - E | |||
: [[contact::L. 620'-6" YY D-513-016 Intermediate Building]], Structural Steel Framing, El. 637', | |||
639'-6", and 642' | |||
C D-412-222-86-0602D, CUN 4805 | |||
Air Instrument Storage Tank Anchorage Details | |||
09/25/1986 302-0271-00000 Piping System Diagram, Safety Related Instrument Air System | |||
S MK-1P57-H1140 Pipe Support Drawing | |||
MK-1P57-H1141 Pipe Support Drawing | |||
2/31/1984 B-208-199 Elementary Diagram 1P57F0015A | |||
N 206-0050-00000 One-line Diagram, Unit 1, Class 1E, Division 3 DC System | |||
Z 256-0050-00000 One-line Diagram, Unit 2, Class 1E, Division 3 DC System | |||
N 302-0358-00000 Div. 3 Diesel starting Air/ Air Dryer Diagram | |||
G 10 CFR 50.59 DOCUMENTS (SCREENINGS/SAFETY EVALUATIONS) | |||
Number Description or Title | |||
Date or Revision ONI-ZZZ-1 50.59 Applicability | |||
Review for CST | |||
Suction Swap to SP for | |||
Tornado/Tornado Warning 05/1993 ONI-ZZZ-1 Tornado or High Winds | |||
06/30/1995 | |||
10 CFR 50.59 DOCUMENTS (SCREENINGS/SAFETY EVALUATIONS) | |||
Number Description or Title | |||
Date or Revision 14-01322 Screening, Installation of Spent Fuel Pool Level Instrumentation for Beyond Design Basis External Events | |||
MISCELLANEOUS | |||
Number Description or Title | |||
Date or Revision E22B SHR 2016 | |||
-3 System - E22B - High Pressure Core Spray Diesel Components | |||
2/02/2017 OE-2012-1550 NRC Information Notices, IN12 | |||
-17 09/17/2012 OT-Combined-P57 Safety Related Instrument Air System (training material) | |||
Qualification Report 108025 Rosemont Pressure Transmitter | |||
D PRS-1700 Technical Requirements for Seismic analysis, Testing and Documentation of Mechanical and Electrical Equipment | |||
System P57 | |||
Maintenance Rule System Basis Document | |||
Engineering Report 84-02 Seismic Qualification Report (for valve 1P57 | |||
-F015B) 03/05/1984 Report WR 83 | |||
-27 Wyle Laboratories Report | |||
- Qualification of Five Motor Operated Valve Assemblies | |||
06/21/1983 600661784 | |||
EER - Evaluate Acceptable Seat Leakage Criteria for 1E22F0538A/B | |||
01/14/2011 N/A Test Protocol | |||
- HPCS Diesel Generator Jacket Water Heat Exchangers | |||
06/11/2012 OE-2015-0025-3 IN15-01 Evaluation, Degraded Ability to Mitigate Flooding Events 01/16/2015 MODIFICATIONS | |||
Number Description or Title | |||
Revision ECP 12-0835-000 Installation of SFP Instrumentation | |||
ECP 00-1120 Part / Component Equivalent Replacement Package | |||
- Torque Switch for Limitorque SMB | |||
-000 Actuators, Clamp Style | |||
ECP 14-0228-001 New EDG Fuel Oil Level Instruments | |||
ECP 09-0573 Emergency Service Water "C" Pump Refurbishment | |||
ECP 11-0755 Place Sand Bags in Control Complex at Door IB | |||
-103 0 | |||
PROCEDURES | |||
Number Description or Title | |||
Revision ARI-H13-P601-0016 DIV 3 Diesel Gen & HPCS | |||
ONI-E12-1 Inadvertent Initiation of ECCS/RCIC | |||
SOI-R44/E22B Division 3 Diesel Generator Starting Air System | |||
SOI-R44 Division 1 and 2 Diesel Generator Starting Air System | |||
ONI-SPI C-2 HPCS System Alignment | |||
SOI-E22A High Pressure Core Spray System | |||
ARI-E22-P001 HPCS Diesel Generator Control Panel | |||
ARI-H13-P601-0016 DIV 3 Diesel Gen & HPCS | |||
ONI-R10 Loss of AC Power | |||
ONI-SPI C-5 Division 3 EDG Restoration | |||
SOI-E22B Division 3 Diesel Generator | |||
SVI-R22-T5069 Division 1 4.16 kV Bus EH11 Degraded Voltage Channel Functional Test | |||
SVI-R22-T5070 Division 2 4.16 kV Bus EH12 Degraded Voltage Channel Functional Test | |||
SVI-R22-T5071 Division 34.16 kV Bus EH13Degraded Voltage Channel Functional Test | |||
SVI-R22-T5072 Division 1 4 kV Bus EH11 Undervoltage/Degraded Voltage Channel Calibration and Logic System Functional Test | |||
SVI-R22-T5073 Division 2 4 kV Bus EH12 Undervoltage/Degraded Voltage Channel Calibration and Logic System Functional Test | |||
SVI-R22-T5074 Division 3 4 kV Bus EH13 Undervoltage/Degraded Voltage Channel Calibration and Logic System Functional Test | |||
NOP-OP-1013 Control of Time Critical Operator Actions | |||
ARI-H13-P601-0019 SRV's Outboard Isolation Valves and Main Steam | |||
SOI-P57 Safety Related Instrument Air Syste | |||
m 17 EOP Bases | |||
Emergency Operating Procedure Bases | |||
EOP-01 RPV Control | |||
EOP-02 Primary Containment Control | |||
EOP-03 Secondary Containment Control | |||
EOP-04 Emergency Depressurization | |||
EOP-SPI 6.4 HPCS Injection | |||
ARI-H13-P877-002 Division 2 Power | |||
ARI-H51-P054B Division 2 Diesel Engine Control Panel | |||
SOI-M43 Diesel Generator Building Ventilation System | |||
SOI-R45 Division 1 and Division 2 Generator Fuel Oil System | |||
ARI-E22-P001 HPCS Diesel Generator Control Panel | |||
ONI-R10-2 Station Blackout B | |||
PROCEDURES | |||
Number Description or Title | |||
Revision ONI-R10-1 Loss of AC Power Flow Chart | |||
A ONI-SPI-C-5 Division 3 EDG Restoration | |||
SOI-R42 Division 3 DC Distribution | |||
ONI-SPI-C-3 CST Transfer to Suppression | |||
NOP-OP-1002 Conduct of Operations | |||
SOI-P45/P49 Emergency Service Water and Screen Wash Systems | |||
ONI-SPI-D-1 Maintaining System Availability | |||
ONI-SPI-D-3 Cross-Tying Unit 1 and 2 Batteries | |||
ONI-SPI-D-9 Makeup Water Sources | |||
SVI-P57-T2001 Safety-Related Instrument Air MOV Operability Test | |||
SVI-P57-T2003 1P57 F015A and 1P57 F020A Remote Shutdown | |||
Position Indication Verification | |||
SVI-R10-T5228 On-Site Power Distribution System Verification | |||
ISI-E22-T1201-3 HPCS Standby Diesel Generator Starting Air System Inservice Pressure Test Class 3 | |||
ISI-R44-T1200-3 Standby Diesel Generator Starting Air System Inservice Pressure Test Class 3 | |||
PTI-E22-P0007 HPCS Diesel Generator Jacket Water Heat | |||
Exchanger Performance Testing | |||
SVI-E22-T2001 HPCS Pump and Valve Operability Test | |||
SVI-R45-T2001 Division 1 Diesel Generator | |||
Fuel Oil Transfer Pump and | |||
Valve and Starting Air Check Valve Operability Test | |||
SVI-R45-T2002 Division 2 Diesel Generator Fuel Oil Transfer Pump and | |||
Valve and Starting Air Check Valve Operability Test | |||
SVI-R45-T2003 Division 3 Diesel Generator Fuel Oil Transfer Pump and Valve and Starting Air Check Valve Operability Test | |||
SVI-E22-T1183 HPCS Valve Lineup Verification and System Venting | |||
SURVEILLANCES (COMPLETED) Number Description or Title | |||
Date PY-ISI-P57T1200-2 Safety Related Instrument Air (SRAI) System Inservice Pressure Test | |||
-Class 2 03/27/2017 PY-ISI-P57T1201-3 Safety Related Instrument Air (SRAI) System Inservice Pressure Test | |||
-Class 3 03/13/2017 PY-ISI-P57T2001-1 Safety Related Instrument Air Motor Operated Valve Operability Test | |||
04/19/2017 PY-ISI-P57T9116 Safety Related Instrument Air (SRAI) System Inservice Pressure Test | |||
-Class 2 03/20/2017 PY-ISI-P57T2001 2 | |||
Safety Related Instrument Air Motor Operated Valve Operability Test (PI) | |||
03/12/2017 | |||
SURVEILLANCES (COMPLETED) Number Description or Title | |||
Date ISI-E22-T1201-3 HPCS Standby Diesel Generator Starting Air System Inservice Pressure Test Class 3 | |||
05/12/2016 ISI-E22-T1201-3 HPCS Standby Diesel Generator Starting Air System Inservice Pressure Test Class 3 11/19/2012 ISI-R44-T1200-3 Standby Diesel Generator Starting Air System Inservice Pressure Test Class 3 | |||
11/19/2012 ISI-R44-T1200-3 Standby Diesel Generator Starting Air System Inservice Pressure Test Class 3 | |||
06/29/2015 PTI-E22-P0007 HPCS Diesel Generator Jacket Water Heat Exchanger Performance Testing | |||
08/04/2008 PTI-E22-P0007 HPCS Diesel Generator Jacket Water Heat Exchanger Performance Testing | |||
2/16/2010 PTI-E22-P0007 HPCS Diesel Generator Jacket Water Heat Exchanger Performance Testing | |||
05/12/2015 SVI-E22-T2001 HPCS Pump and Valve Operability Test | |||
2/06/2017 WORK DOCUMENTS | |||
Number Description or Title | |||
Date 200513404 | |||
Perform Static Test/Limitorque | |||
Maintenance (PMI | |||
-0030) 03/22/2015 200061492 | |||
Perform Static Test/Limitorque Maintenance (PMI | |||
-0030) 03/15/2005 200680513 | |||
Perform Operability Test of 1P57F0015 A & B | |||
04/19/2017 200279346 | |||
Month Performance Test of Unit 1, Division 3 Battery Capacity 08/05/2013 200600623 | |||
Month Service Test of Unit 1, Division 3 Battery Capacity | |||
2/16/2016 200680607 | |||
Day Unit 1, Division 3 Battery Category B Limits, Terminal Corrosion and Electrolyte Temperature Check | |||
05/11/2017 200660494 | |||
On-Site Power Distribution System Verification | |||
06/11/2017 200061492 | |||
Perform Full PMI | |||
-0030 on MOV 1P57F0015B | |||
03/15/2005 | |||
LIST OF ACRONYMS USE | |||
D CAP Corrective Action Program | |||
CFR Code of Federal Regulations | |||
CR Condition Report | |||
CST Condensate Storage Tank | |||
ECP Engineering Change Package | |||
EDG Emergency Diesel Generator | |||
EOP Emergency Operating Procedure | |||
ESW Emergency Service Water | |||
HPCS High Pressure Core Spray | |||
IMC Inspection Manual Chapter | |||
IN Information Notice | |||
LERF Large Early Release Frequency LOOP Loss of Off | |||
-site Power | |||
NCV Non-Cited Violation | |||
NRC U.S. Nuclear Regulatory Commission | |||
RCIC Reactor Core Isolation Cooling | |||
SBO Station Blackout | |||
SDP Significance Determination Process | |||
SPAR Standardized Plant Analysis Risk | |||
SRA Senior Reactor Analyst UFSAR Updated Final Safety Analysis Report | |||
}} | }} |
Revision as of 05:15, 29 June 2018
ML18004B072 | |
Person / Time | |
---|---|
Site: | Perry |
Issue date: | 01/03/2018 |
From: | Jeffers M T NRC/RGN-III/DRS/EB2 |
To: | Hamilton D B FirstEnergy Nuclear Operating Co |
References | |
IR 2017008 | |
Download: ML18004B072 (37) | |
Text
UNITED STATES NUCLEAR REGULATORY COMMISSION REGION III 2443 WARRENVILLE RD. SUIT E 210 LISLE, ILLINOIS 60532
-4352 January 3, 2018 Mr. David B. Hamilton Site Vice President FirstEnergy Nuclear Operating Company Perry Nuclear Power Plant Reg Affairs
-A210 10 Center Road, P.O. Box 97 Perry, OH 44081
-0097
SUBJECT: PERRY NUCLEAR POWER PLANT
-NRC DESIGN BASES ASSURANCE INSPECTION (TEAMS) INSPECTION REPORT 05000440/
2017008 Dear Mr. Hamilton
- On September 14, 2017, the U.S. Nuclear Regulatory Commission (NRC) completed a triennial baseline Design Bases Assurance Inspection (Team s) at your Perry Nuclear Power Plan The enclosed report documents the results of this inspection, which were discussed on November 22, 2017, with Mr. Conicella, and other members of your staf Three NRC-identified findings of very
-low safety significance were identifie The findings involved violation s of NRC requirement However, because of their very-low safety significance, and because the issues were entered into your Corrective Action Program, the NRC is treating the issues as Non-Cited Violations in accordance with Section 2.3.2 of the NRC Enforcement Polic If you contest the violations or significance of these Non-Cited Violations, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555 0001; with copies to the Regional Administrator, Region III; the Director, Office of Enforcement; and the NRC resident inspector at the Perry Nuclear Power Plant
. If you disagree with a cross
-cutting aspect assignment or a finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555
-0001; with copies to the Regional Administrator, Region III
- and the NRC resident inspector at the Perry Nuclear Power Plan D. Hamilton
-2- This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading
-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, "Public Inspections, Exemptions, Requests for Withholding."
Sincerely,/RA/ Mark T. Jeffers, Chief Engineering Branch 2 Division of Reactor Safety Docket N License No. NPF
-58
Enclosure:
IR 05000440/2017008 cc: Distribution via LISTSERV
SUMMARY
Inspection Report 05000440/2017008
, 08/14/2017-09/14/2017; Perry Nuclear Power Plant
- Design Bases Assurance Inspection (Teams). The inspection was a 2
-week onsite baseline inspection that focused on the design of components and modifications to mitigating systems. The inspection was conducted by regional engineering inspectors and two consultants. The inspection team identified three findings of very-low safety significance (Green) associated with Non-Cited Violations (NCVs) of U.S. Nuclear Regulatory Commission (
NRC) regulations. The significance of inspection findings is indicated by their color (i.e., Green, White, Yellow, and Red) and determined using Inspection Manual Chapter 0609, "Significance Determination Process
," dated April 29, 2015. Cross-Cutting aspects are determined using Inspection Manual Chapter 0310, "Aspects Within the Cross-Cutting Areas
," dated December 4, 2014. All violations of NRC requirements are dispositioned in accordance with the NRC's Enforcement Policy, dated November 1, 2016. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG
-1649, "Reactor Oversight Process
," Revision 6, dated July 2016
.
NRC-Identified
and Self-Revealed Findings
Cornerstone: Mitigating Systems
- Green.
The team identified a finding of very-low safety significance (Green) and an associated NCV of Title 10 of the Code of Federal Regulations (CFR), Part 50, Appendix B, Criterion III, "Design Control," and 10 CFR 50.63, "Loss of All Alternating Current Power," for the licensee's failure to evaluate the capability to transfer the high pressure core spray (HPCS) and the reactor core isolation cooling (RCIC) pumps' suction source from the condensate storage tank (C ST) to the suppression pool during cold weather conditions. Specifically, (1) monitoring of the CST level instrument lines heat tracing was inadequate to detect a credible common mode failure before the instrument lines would freeze and be rendered inoperable during normal operation, (2)the licensee did not address the condensate (CST) level instrument lines susceptibility to freeze during a cold weather loss of off-site power (LOOP) event with or without a design basis transient or accident, and (3) the licensee incorrectly evaluated the capability to transfer the HPCS pump suction source from the CST to th e suppression pool during a cold weather station blackout (SBO) event. The licensee captured the issues within their Corrective Action Program (CAP) as Condition Report (CR) CR-2017-08685, CR
-2017-08930, and CR
-2017-09006. Corrective actions implemented included:
increased the CST level instrument line heat tracing circuit monitoring frequency, revise d the affected procedures ensure d HPCS and RCIC are adequately aligned to the suppression pool during LOOP design basis events, and ensured a timely transfer of the HPCS and RCIC pump suctions to the suppression pool during a SBO.
The performance deficiency was determined to be more-than-minor because it was associated with the Mitigating Systems cornerstone attribute of design control and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.
Specifically, the failure of the HPCS and or RCIC pumps to automatically transfer their suction source from the CST to the suppression pool upon reaching a low CST water level condition could damage the pump(s) thus preventing them to be used to mitigate a transient or accident.
A detailed risk evaluation was performed and determined that the finding was of very-low safety- significance (Green). The team did not identify a cross-cutting aspect associated with this finding because it was not confirmed to reflect current performance due to the age of the performance deficiency. Specifically, the CST instrument lines were designed and the SBO coping strategy during cold weather was established more than years ago.
(Section 1R21.3.b(
1))
- Green.
The team identified a finding of very-low safety significance (Green) and an associated NCV of 10 CFR Part 50, Appendix B, Criterion III, "Design Control," for the failure to consider all stresses resulting from the emergency closed cooling system as built pipe support 1P42
-H1080 connection details. Specifically, the evaluation for the pipe support did not address the impact of rigid connections at both ends of the W8 steel post and of the lateral load on W21 auxiliary steel beam. The licensee captured the issues in their CAP as CR
-2017-08986 and CR
-2017-09043, reasonably determined the support remained operable, and planned to revise the affected structural analyses.
The performance deficiency was determined to be more-than-minor because it was associated with the Mitigating Systems cornerstone attribute of design control and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.
Specifically, the failure to analyze actual pipe configuration and to evaluate the W21 beam did not ensure the emergency closed cooling system and its safety-related supported loads would remain available and capable of providing their accident mitigating function. The finding screened as of very-low safety significance (Green) because it did not result in the loss of operability or functionality of mitigating systems. The team determined that this finding had a cross-cutting aspect in the area of human performance because the licensee did not recognize and plan for the possibility of mistakes, latent issues, and inherent risk, even while expecting successful outcomes. Specifically, the licensee did not recognize this latent issue when revising the structural evaluation in 2015.
(Section 1R21.4.b(1))
[H.12]
- Green.
The team identified a finding of very-low safety significance (Green) and an associated NCV of 10 CFR Part 50, Appendix B, Criterion III, "Design Control," for the failure to verify the capability to manually backwash the emergency service water (ESW) strainer during a LOOP. Specifically, the licensee credited the capability to manually backwash the ESW strainers during a LOOP. However, the associated differential pressure alarm setpoint did not ensure sufficient time to complete this activity because the alarms were set at the same value as the design differential pressure value assumed by the hydraulic calculations. The licensee captured the issue in their CAP as CR-2017-09033, reasonably determined ESW remained operable, and planned to revise the associated calculation and the alarm setpoint to ensure sufficient time to perform the required manual actions during a LOOP.
4 The performance deficiency was determined to be more-than-minor because it was associated with the Mitigating Systems cornerstone attribute of protection against external factors and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the performance deficiency did not assure the ESW capability to supply the required minimum flow to its supported components. The finding screened as of very-low safety significance (Green) because it did not result in the loss of operability or functionality of mitigating systems. The team did not identify a cross-cutting aspect associated with this finding because it was not confirmed to reflect current performance due to the age of the performance deficiency. Specifically, the alarm setpoint was established more than years ago. (Section 1R21.6.b(2))
5
REPORT DETAILS
REACTOR SAFETY
Cornerstone s: Initiating Events, Mitigating Systems, and Barrier Integrity
1R21 Design Bases Assurance Inspection (Team
s) (71111.21 M)
.1 Introduction
The objective of the design bases assurance inspection is to verify that design bases have been correctly implemented for the selected risk
-significant components and modifications, and that operating procedures and operator actions are consistent with design and licensing bases. As plants age, their design bases may be difficult to determine and an important design feature may be altered or disabled during a modification. The inspection also monitors the implementation of modifications to structures, systems, and components as modifications to one system may also affect the design bases and functioning of interfacing systems as well as introduce the potential for common cause failures. The Probabilistic Risk Assessment model assumes the capability of safety systems and components to perform their intended safety function successfully. This inspect able area verifies aspects of the Initiating Events, Mitigating Systems, and Barrier Integrity cornerstones for which there are no indicators to measure performance.
Specific documents reviewed during the inspection are listed in the to the report.
.2 Inspection Sample Selection Process
The team used information contained in the licensee's Probabilistic Risk Assessment and the Perry Nuclear Power Plant Standardized Plant Analysis Risk (SPAR) Model to identify one scenario to use as the basis for component selection. The scenario selected was a loss of offsite power (LOOP) event. Based on this scenario, a number of risk-significant components, including those with Large Early Release Frequency (LERF) implications, were selected for the inspection.
The team also used additional component information such as a margin assessment in the selection process. This design margin assessment considered original design reductions caused by design modification s, power uprates, or reductions due to degraded material condition. Equipment reliability issues were also considered in the selection of components for detailed review. These included items such as performance test results, significant corrective actions, repeated maintenance activities, Maintenance Rule (a)(1) status, components requiring an operability evaluation, system health reports, and U.S. Nuclear Regulatory Commission (
NRC) resident inspector input of problem areas/equipment. Consideration was also given to the uniqueness and complexity of the design, operating experience, and the available defense in depth 6 margins. A summary of the reviews performed and the specific inspection findings identified are included in the following sections of the report.
The team also identified modifications for review. In addition, the inspectors selected procedures and operating experience issues associated with the selected components.
This inspection constituted 13 samples (
6 components with 1 component associated with LERF implications, 4 modifications, and 3 operating experience) as defined in Inspection Procedure 71111.21M
-02.01.
.3 Component Design
a. Inspection Scope
The team reviewed the Updated Final Safety Analysis Report (U FSAR), Technical Specifications, design basis documents, drawings, calculations and other available design basis information, to determine the performance requirements of the selected components. The team used applicable industry standards, such as the American Society of Mechanical Engineers Code, Institute of Electrical and Electronics Engineers Standards
, and the National Electric Code, to evaluate acceptability of the systems' design. The NRC also evaluated licensee actions, if any, taken in response to NRC issued operating experience, such as Bulletins, Generic Letters, Regulatory Iss ue Summaries, and Information Notices (INs). The review was to verify that the selected components would function as designed when required and support proper operation of the associated systems. The attributes that were needed for a component to perform its required function included process medium, energy sources, control systems, operator actions, and heat removal. The attributes to verify that the component condition and tested capability was consistent with the design bases and was appropriate may have included installed configuration, system operation, detailed design, system testing, equipment and environmental qualification, equipment protection, component inputs and outputs, operating experience, and component degradation.
For each of the components selected, the inspectors reviewed the maintenance history, preventive maintenance activities, system health reports, operating experience
-related information, vendor manuals, electrical and mechanical drawings, operating procedures, and licensee
's Corrective Action Program (CAP) documents. Field walkdowns were conducted for all accessible components selected to assess material condition, including age-related degradation, configuration, potential vulnerability to hazards, and consistency between the as
-built condition and the design. In addition, the team interviewed licensee personnel from multiple disciplines such as operations, engineering, and maintenance. Other attributes reviewed are included as part of the scope for each individual component.
The following six components (samples), including a component with LERF implications, were reviewed
Division 3 Emergency Diesel Generator (EDG) (1E22C0001)
- The team reviewed the mechanical aspects of the EDG design, including the air starting system, the fuel oil storage and transfer system, and the jacket water cooling system to assess the capability of the EDG to perform its design function under accident and transient conditions. The team reviewed the protection of the EDG and associated equipment from external events, including flooding. The team reviewed the availability of jacket water cooling under LOOP and station blackout (SBO) conditions. The team reviewed the generator circuit diagrams, field winding circuit, grounding scheme, fuel oil transfer pump circuitry, and control logic. The team reviewed the short circuit current calculation data and results, and the coordination calculation to assess the short circuit duty and the coordination between the generator and the motor and transformer loads including ratings and branch circuit cabling. The team also reviewed voltage drop, loading sequence, minimum and maximum voltage profiles, and the impact of the changes in voltage and frequency. The calculation review verified methodology, design inputs, assumptions, and results.
The team also reviewed jacket water cooling and air start system test procedures and recent test results.
High-Pressure Core Spray (HPCS) Pump (1E22C0001)
- The team reviewed the following HPCS hydraulic calculations to assess the pump capability to perform its required mitigating functions: pump minimum required flow, runout flow, flow capacity, and minimum required net positive suction head. In addition, the team reviewed the suction sources of the pump and the instrumentation associated with the automatic transfer of the sources. The team reviewed the operation of the HPCS pump under accident, transient, SBO, and external event conditions to assess its capability to perform its licensing basis functions. The team reviewed the room cooling associated with the pump to assess the pump's operating environment. The team reviewed electrical calculations, drawings and equipment modifications to assess the availability of the voltage and current at the pump motor terminals for starting and running under worst case design basis loading, operation on emergency power, and grid voltage conditions. In addition, the team reviewed the control logic, protective relay settings, and cable short circuit current to assess the electrical protection coordination and the power supply feeder cables sizing.
The team also reviewed surveillance test procedures and recent test results.
Division 2
, Safety-Related Instrument Air Containment Isolation Valve (1P57F0015B): The team reviewed the installed configuration of the valve and adjacent pipe supports to verify conformance with the applicable drawings. In addition, the team reviewed the seismic qualification documentation for the valve to assess its seismic qualification; power and control wiring drawings, and voltage drop calculation to assess the availability of the minimum required voltage to the valve under all postulated conditions; and sizing for the cables and fuses. The team also reviewed the system operating procedures, design modifications, maintenance rule documentation, system health reports, periodic 8 maintenance activities, and operability tests, including in-service testing records.
This review constituted one component sample with LERF implications.
Safety-Related Instrument Air Storage Tank B (1P57A0003B): The team reviewed calculations related to the storage tank capacity, including the minimum allowable pressure and the allowable leakage limits to assess its capacity under the most limiting conditions. The team reviewed seismic anchorage calculation for the tank and the seismic qualification documentation for the instruments. In addition, the team reviewed the associated instrumentation details and the calibration records of the pressure transmitters. The team also reviewed the system operating instructions and testing records.
Division 3, 480V Motor Control Centers EF1E-1/2 (1R24S0029/30): The team reviewed the elementary diagram to assess the sizing of control and power fuses and the cables. Also, the voltage drop calculation was reviewed to assess the availability of power and control voltage to the loads and the control components under all postulated conditions. The team also reviewed the design of the associated power supply fuses and the individual load fuses to assess their coordination.
HPCS Battery and Charger (1E22S0006 and EFD
-1C): The team reviewed calculations and analyses related to battery loads, battery and charger sizing and capacity, hydrogen generation, and battery room temperature. The review was performed to assess the battery and charger capability to support the design basis required voltage requirements of the 125 Vdc Division 3 safety
-related loads under both normal and design basis accident conditions.
The team also reviewed a sample of completed surveillance tests, service duty discharge tests, and modified performance tests.
b. Findings
(1) Failure to Address the Susceptibility of the Condensate Storage Tank Low Level Instrument Lines to Freeze Introduction
- The team identified a finding of very
-low safety significance (Green)and an associate d Non-Cited Violation (
NCV) of Title 10 of the Code of Federal Regulations (CFR), Part 50, Appendix B, Criterion III, "Design Control," and 10 CFR 50.63, "Loss of All Alternating Current Power," for the licensee's failure to evaluate the capability to transfer the HPCS and the reactor core isolation cooling (RCIC) pumps' suction source from the condensate storage tank (CST) to the suppression pool during cold weather conditions. Specifically, (1) monitoring of the CST level instrument lines heat tracing was inadequate to detect a credible common mode failure before the instrument lines would freeze and be rendered inoperable during normal operation, (2) the licensee did not address the condensate (CST) level instrument lines susceptibility to freeze during a cold weather LOOP event with or without a design basis transient or accident, and (3) the licensee incorrectly evaluated the capability to transfer the HPCS pump suction source from the CST to the suppression pool during a cold weather station blackout (SBO) event.
9 Description
- The CST low level instruments are relied upon to transfer the suctions of HPCS and RCIC to the suppression pool before CST water level would result in inadequate submergence (i.e., inadequate net positive suction head and/or vortexing).
The CST level instruments are controlled under Technical Specification 3.3.5.1, "Emergency Core Cooling Instrumentation
," and are credited in the SBO analysis to ensure that an assumed volume of water from the CST is added to the suppression pool to manage suppression pool heat up during the licensed 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> coping period without preferred or emergency power. The instrument lines are exposed to the outside environment and rely on heat tracing and insulation to prevent freezing during cold weather conditions. The heat tracing circuit is not safety
-related and not powered by the emergency power sources.
The team identified the following three examples were the licensee did not address the susceptibility of the CST low level instrument lines to freeze affecting the capability to transfer HPCS and RCIC pumps' suction from the CST to the suppression pool under various cold weather conditions:
The team identified that the licensee failed to address the susceptibility of the CST low level lines to freeze during normal operating conditions
. Specifically, the instrument lines heat tracing circuits were susceptible to common mode failure since the circuits were connected to the same electrical cabinet and the expected time to freeze the instrument lines (e.g., less than 90 minutes in some cases) was significantly shorter than the periodic operator rounds (e.g., every 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> in most cases)that include verifying that the heat trace circuit is operating properly. Thus, the monitoring of the heat tracing circuit was, therefore, inadequate to ensure that the HPCS and RCIC pump suctions were capable to transfer from the CST to the suppression pool during cold weather because the monitoring frequency would not result in the timely detection of a heat trace circuit failure before a loss of function could occur
. The team identified that the licensee failed to address the susceptibility of the CST low level instrument lines to freeze during design basis LOOP conditions. Specifically, the design did not recognize that the CST level instrument lines would not support HPCS and RCIC suction transfer during a LOOP with cold weather because the heat tracing were not powered by the E DGs.
The team identified that the evaluation of the SBO coping strategy was not technically correct because it non
-conservatively estimated the times to freeze the CST low level instrument lines and transfer the HPCS suction. In this case, the licensee had previously recognized that the design of the CST low level instrument lines would not prevent freezing during an SBO with cold weather because the insulated lines were exposed to the outside environment and their heat trace circuit would not be powered during an SBO. As a result, the licensee developed an SBO coping strategy intended to protect the HPCS and RCIC pumps from inadequate submergence by transferring the entire CST usable volume to the suppression pool before the CST level instrument lines would freeze. This transfer included both the normal transfer through the vessel duri ng normal post reactor trip operations to maintain reactor vessel water level as well 10 as an expedited operation to transfer the CST directly to the suppression pool when reactor vessel makeup was not necessary. This transfer would result in an automatic HPCS and RCIC pump suction swap from the CST to the suppression pool upon reaching a low CST water level
. While the SBO coping analysis only credited HPCS, the plant's procedures treated the RCIC system as the preferred system. However, the team identified that
- The time allotted for pump suction transfer from the CST to the suppression pool was based on a calculation that assumed the instruments remained functional with a small active water volume that was judged by the team to be inadequate. Specifically, the calculation determined the time to freeze the 3/8 inch outside diameter instrument line such that the unfrozen diameter is 1/16 inch (i.e., the unfrozen 1/16 inch core was credited to sense CST level). The 1/16 inch unfrozen diameter was judged by the team to be inadequate because the mathematical model was based on ideal and uniform assumptions that were not applicable to the actual field configuration exposed to non-controlled environmental conditions. In addition, the existence of a relatively small dimension deviation from the assumed dimension value (e.g., an elbow, valve internals, kink on the line, slight deformation due to handling) could exist leading to a freeze seal prior to the estimated freezing time. This non
-conservatism was further exacerbated by significant calculational errors. Specifically, the calculation assumed the instrument lines were perfectly insulated. However, the team identified during a field walk down that the actual insulation was crushed adversely affecting the calculation assumptions regarding insulation thickness and thermal conductivity values. In addition, the calculation did not consider uninsulated valves and angle iron supports extending out of the insulation acting as heat transfer fins which would bypass the insulation
. The evaluation of this strategy underestimated the time to transfer the entire CST usable volume and the pumps' suctions to the suppression pool. Specifically, the licensee estimated that this transfer would occur around 30
-40 minutes after the SBO initiation. The licensee considered this timeframe acceptable because they estimated (non
-conservatively as previously discussed) about 83 and 106 minutes to freeze the instrument line assuming ambient temperatures of
-10 degrees Fahrenheit and 0 degrees Fahrenheit, respectively. However, the team noted the transfer time was estimated using less than the usable CST volume instead of the entire CST usable volume as directed by plant procedures. The team estimated that the transfer of the entire CST usable volume would take approximately 93 minutes based on a reasonable extrapolation of a scenario the team observed at the control room simulator.
The licensee captured the issues within their CAP as Condition Report (
CR) CR-2017-08685, CR
-2017-08930, and CR
-2017-09006. Planned corrective actions to be implemented during the next cold weather condition included: an action to increase the CST level instrument line heat tracing circuit monitoring frequency, revise the affected procedures to ensure HPCS and RCIC are adequately aligned to the 11 suppression pool during LOOP design basis events, and to ensure a timely transfer of the HPCS and RCIC pump suctions to the suppression pool during a SBO.
Analysis:
The team determined that the failure to evaluate the capability to transfer HPCS and RCIC pumps suctions from the CST to the suppression pool under cold weather conditions was contrary to 10 CFR Part 50, Appendix B, Criterion III, "Design Control," and 10 CFR 50.63, "Loss of All Alternating Current Power," and was a performance deficiency. The performance deficiency was determined to be more-than-minor because it was associated with the Mitigating Systems cornerstone attribute of design control and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the failure of the HPCS and or RCIC pumps to automatically transfer their suction source from the CST to the suppression pool upon reaching a low CST water level condition could damage the pump(s) thus preventing them to be used to mitigate a transient or accident.
The team determined the finding could be evaluated using the Significance Determination Process (SDP) in accordance with Inspection Manual Chapter (IMC) 0609, "Significance Determination Process," Attachment 0609.04, "Initial Characterization of Findings," issued on October 7, 2016. Because the finding impacted the Mitigating Systems cornerstone, the inspectors screened the finding through IMC 0609 Appendix A, "The Significance Determination Process for Findings At
-Power," issued on June 19, 2012, using Exhibit 2, "Mitigating Systems Screening Questions." The team determined the finding required a detailed risk evaluation because the available information provided by the licensee as of September 15, 2017, did not demonstrate reasonable assurance that the HPCS and RCIC pumps would have remained functional with cold weather. Specifically, the team determined that the expected time to freeze the instrument lines was less than the time to reach the CST low level setpoint associated with the pumps suction transfer. .
The Senior Reactor Analyst (SRA) performed a detailed risk evaluation using a version of the Perry SPAR Model, Revision 8.19, which had recently been modified with some additional plant specific features that are documented in Inspection Report 05000440/
2017009. The SRA requested that Idaho National Laboratory slightly modify this revision of the SPAR model to include a basic event modeling the potential for operator action to perform the suction transfer of the HPCS and RCIC systems from the CST to suppression pool if it failed to occur. In the base model, the newly added operator action failure probability was set to 2E
-2. This human error probability was estimated using the SPAR Human Reliability Analysis Method for the baseline risk by assuming that the operator failure would be dominated by diagnosis errors and that the only performance driver was a performance shaping factor of High Stress. For this human error probability evaluation, all alarms, instruments, etc. are assumed to function normally and are not affected by the freezing condition. For the degraded condition, the instrument freezing may both prevent the automatic transfer and hinder operator diagnosis of the condition by indicating a false high level in the CST when level is actually decreasing.
12 To estimate the change in risk due to the degraded condition, the following assumptions were made:
The degraded condition was modeled as a recoverable failure of the automatic suction transfer function of the HPCS and RCIC systems.
Only the loss of offsite power event trees were evaluated. The level indication and automatic suction swap
-over of the systems remained available for other initiating events.
The CST level instruments and level sensors required for successful suction transfer of HPCS and RCIC from the CST to the suppression pool are not modeled in the SPAR model. The SRA used two existing basic events in the SPAR model as surrogates to represent failure of the automatic suction transfer due to freezing. For the HPCS system, the basic event HCS
-MOV-FT-SUCTR, "HPCS Suction Transfer Fails" was set to "True" or failed. For the RCIC system, the basic event "RCI
-MOV-OO-F010" was also set to "True" or failed.
The basic event for operator action to perform the suction transfer of both systems was evaluated using the SPAR Human Reliability Method.
The SRA assumed the performance shaping factor that would be the most significant performance driver in the degraded condition was ergonomics, as the indication of CST level necessary for diagnosis could be misleading. However, the SRA also determined that operators would be monitoring level, and could determine that the low CST level should have been reached and take the necessary manual action. The ergonomics performance shaping factor was rated as "poor". All other performance shaping factors were set at the nominal values. The resulting human error probability for the failure to perform the suction transfer was 0.2.
The exposure period was determined to be 58 days. This was based on the past 3 years of weather data reviewed by the licensee to determine, on average, the number of days that the outside temperature was less than 32 degrees Fahrenheit. This is likely a conservative estimate of the exposure period. The UFSAR Table 2.3-3 showed the mean number of days with a high of 32 degrees Fahrenheit as 36 degrees Fahrenheit. The exposure time was further divided into a period of 13 days, which represents the mean time below 17 degrees Fahrenheit, and 45 days, the mean time with a temperature above 17 degrees Fahrenheit but below 32 degrees Fahrenheit. Below 17 degrees Fahrenheit
, plant SBO procedures require using the HPCS system to transfer water from the CST to the suppression pool, which results in a much shorter time to the low CST level and possible pump damage. However, above 17 degrees Fahrenheit, this action is not required, and the time to the low level in the CST would be similar to the LOOP scenarios.
The CST is normally maintained with approximately 400,000 gallons of water. The low level CST alarm and automatic suction transfer should normally occur at approximately 98,000 gallons. The RCIC is the preferred system over HPCS for use during LOOP events. Assuming a RCIC flowrate of 700 gpm, many hours of successful operation would occur before any concern with loss of suction a nd 13 pump trip. This time would allow for the recovery of offsite power and the use of normal inventory control and heat removal systems. To account for the recovery of offsite power and use of normal systems, the SRA multiplied the delta core damage frequency for LOOP scenarios by the appropriate offsite power non-recovery probability at 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. For the portion of the exposure period between 17 degrees Fahrenheit and 32 degrees Fahrenheit (i.e., 45 days), offsite power non
-recovery probabilities were also modified for SBO sequences. No additional recovery of offsite power was credited for LOOP or SBO sequences which also involved one or more stuck open relief valves.
The change core damage frequency from the degraded plant condition was estimated as 7E-7/yr. The dominant sequence involved a SBO event, the failure of the operator to perform the suction transfer resulting in RCIC and HPCS failure, and the failure to recover offsite power. External events were evaluated qualitatively using the risk insights from a previous detailed risk evaluation documented in Inspection Report 05000440/2017009. In that evaluation, the external event risk for LOOP related scenarios was less than the internal event risk, primarily because of a lower external event LOOP frequency obtained from the Individual Plant Examination of External Events. The SRA concluded external event risk would not cause the risk of the finding to exceed the 1E
-6/yr. threshold for a more significant finding. The SRA evaluated LERF by applying a 0.2 LERF factor specified by IMC 0609 Appendix H, "Containment Integrity Significance Determination Process," for plants with a Mark III containment to sequences that represent core damage at high pressure. The delta LERF estimate was determined to be less than 1E
-7/yr. Based on the results of the detailed risk evaluation, the finding was determined to be of very
-low safety significance (Green).
The team did not identify a cross
-cutting aspect associated with this finding because it was not confirmed to reflect current performance due to the age of the performance deficiency. Specifically, the CST instrument lines were designed and the SBO coping strategy during cold weather was established more than 3 years ago.
Enforcement:
Title 10 CFR Part 50, Appendix B, Criterion III, "Design Control," states, in part, that measures shall be established for verifying or checking the adequacy of design, such as by the performance of design reviews, by the use of alternate or simplified calculational methods, or by the performance of a suitable testing program.
As of August 23, 2017, the licensee failed to verify the adequacy of design. Specifically, the licensee did not verify the adequacy of the CST low level instruments lines to detect low water level and cause an automatic HPCS and RCIC suction transfer to the suppression pool when the CST supply becomes exhausted during cold weather conditions. The heat tracing of these lines would not provide freeze protection during a 14 LOOP with cold weather and monitoring of the heat tracing was inadequate to detect a failure before the instrument lines estimated freeze time during normal operations with cold weather.
In addition, 10 CFR 50.63, "Loss of All Alternating Current Power," requires, in part, that the licensee determine the capability for coping with an SBO of a specified duration by an appropriate coping analysis. Revision 12 of Section 15H, "Station Blackout
," of the UFSAR, states "The Perry specific SBO assessment which conforms to 10 CFR 50.63 and Regulatory Guide 1.155 follows." Regulatory Guide 1.155, "Station Blackout," Section 3.2, "Evaluation of Plant
-Specific Station Blackout Capability," stated "The following considerations should be included when determining the plant's capability to cope with a station blackout- The design adequacy and capability of equipment needed to cope with a station blackout for the required duration and recovery period should be addressed and evaluated as appropriate for the associated environmental conditions."
It also stated
, "This should include consideration as appropriate of the following- Potential effects of other hazards, such as weather, on station blackout response equipment-"
As of August 31, 2017, the licensee failed to determine the capability for coping with an SBO by an appropriate coping analysis. Specifically, the coping analysis for an SBO with cold weather incorrectly evaluated the capability to transfer the HPCS suction from the CST to the suppression pool because the licensee underestimated the times to (1) freeze the CST low level instrument lines and (2) transfer the entire CST usable volume and the pump suction to the suppression pool.
The licensee has taken corrective actions to address the finding by monitoring the CST level line heat trace circuits more frequently during normal cold weather operating conditions, updating procedures to alert operators that a loss of power to distribution panel F1A04 will result in a loss of CST level line heat tracing, and to ensure that the HPCS and RCIC suction sources are transferred to the suppression pool before the level lines become non
-functional during cold weather design basis and SBO conditions.
Because this violation was of very
-low safety significance (Green) and was entered into the licensee's CAP as CR
-2017-08685, CR
-2017-08930, and CR
-2017-9006 these violations are being treated as an NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy. (NCV 05000440/2017008
-01; Failure to Address the Susceptibility of the C ondensate Storage Tank Low Level Instrument Lines to Freeze)
.4 Mitigating System Modifications
a. Inspection Scope
The team reviewed four permanent plant modifications. This review included in
-plant walkdowns for accessible portions of the modified structures, systems, and components
. The team reviewed the modifications to verify that the design bases, licensing bases, 15 and performance capability of the components had not been degraded through modifications. The modifications were selected based upon risk significance, safety significance, and complexity. The team reviewed the modifications selected to determine if:
the supporting design and licensing basis documentation was updated; the changes were in accordance with the specified design requirements; the procedures and training plans affected by the modification have been adequately updated; the test documentation as required by the applicable test programs has been updated; and post-modification testing adequately verified system operability and/or functionality. The team also used applicable industry standards to evaluate acceptability of the modifications. The modifications listed below were reviewed as part of this inspection effort: Addenda A-01 and A-02 to Revision 9 of Calculation 0P42
-0111, "Self-Weight Excitation Review of Hangers for Emergency Closed Cooling System;
" Engineering Change Package (ECP) 14-0228-001, "New EDG Fuel Oil Level Instruments;"
ECP 09-0573, "Emergency Service Water 'C' Pump Refurbishment;" and ECP 11-0755, "Place Sand Bags in Control Complex at Door IB
-103."
b. Findings
(1) Inadequate Evaluation of Emergency Closed Cooling System Pipe Support
Introduction:
The team identified a finding of very
-low safety significance (Green) and an associated NCV of 10 CFR Part 50, Appendix B, Criterion III, "Design Control," for the failure to consider all stresses resulting from the as built pipe support connection details. Specifically, the evaluation for pipe support 1P42
-H1080 did not address the impact of rigid connections at both ends of the W8 steel post and of the lateral load on W21 auxiliary steel beam.
Description:
In 1985, the licensee evaluated the safety
-related emergency closed cooling system pipe support 1P42
-H1080 in Calculation 0P42
-0111, Revision 9. The calculation was revised through addenda A
-01 and A-02, on September 4, 2014, and September 25, 2015, respectively, to evaluate the addition of conduits associated with the spent fuel pool instrumentation modification.
During this inspection, the team noted that the pipe support configuration consisted of a vertical W31 steel post installed at elevation 620 feet in the intermediate building with the top end rigidly attached to the bottom of the floor at the 654 foot elevation. Thus, in case of any differential vertical displacements between the two floors due to change in live 16 loads or under a seismic event, this configuration would result in a significant transfer of the floor loading to the post. However, Calculation 0P42
-0111, including its addenda A-01 and A-02, did not address this configuration. Specifically, it failed to account for the additional loads associated with the relative displacements of the floors.
The licensee captured this concern in their CAP as CR
-2017-08986 on August 30, 2017.
In addition, the team noted that the post was laterally supported at about mid
-height through a brace to a W21 beam originally installed as an auxiliary steel member to support cable trays. Calculation 0P42
-0111 concluded that the associated stresses in W21 beam would be small and acceptable based on judgment. However, the licensee did not document a basis supporting this judgement and a preliminary review by the team and the licensee during this inspection period determined that the stresses could be significant enough to necessitate more detailed analysis. The licensee captured this concern in their CAP as CR
-2017-09043 on August 31, 2017.
The licensee's immediate corrective actions included an evaluation that reasonably concluded that after consideration of the relative displacements between the floors and with more refined evaluations, the stresses in the pipe support members and the W21 steel beam will remain within the operability limits. The proposed corrective actions to restore compliance at the time of this inspection was to re
-evaluate the structural analyses.
Analysis:
The team determined the failure to consider all stresses resulting from the as built pipe support connection was contrary to 10 CFR Part 50, Appendix B, Criterion III, "Design Control," and was a performance deficiency. The performance deficiency was determined to be more
-than-minor because it was associated with the Mitigating Systems cornerstone attribute of design control and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the failure to analyze actual pipe configuration and to evaluate the W21 beam did not ensure the emergency closed cooling system and its safety-related supported loads would remain available and capable of providing their accident mitigating function.
The team determined the finding could be evaluated using the SDP in accordance with IMC 0609, "Significance Determination Process," Attachment 0609.04, "Initial Characterization of Findings," issued on October 7, 2016. Because the finding impacted the Mitigating Systems cornerstone, the inspectors screened the finding through IMC 0609 Appendix A, "The Significance Determination Process for Findings At
-Power," issued on June 19, 2012, using Exhibit 2, "Mitigating Systems Screening Questions."
The finding screened as of very
-low safety significance (Green) because it did not result in the loss of operability or functionality of mitigating systems. Specifically, the licensee performed an operability determination which concluded that the differential movements between the floors would be very small and that the resulting stresses would reasonably be bounded by the applicable stress operability limits. Licensee evaluation also indicated that the W21 beam stresses would meet the applicable operability limits.
17 The team determined that this finding had a cross
-cutting aspect in the area of human performance because the licensee did not recognize and plan for the possibility of mistakes, latent issues, and inherent risk, even while expecting successful outcomes. Specifically, the licensee did not recognize this latent issue when revising the structural evaluation in 2015.
[H.12]
Enforcement:
Title 10 CFR Part 50, Appendix B, Criterion III, "Design Control," states, in part, that measures shall be established for verifying or checking the adequacy of design, such as by the performance of design reviews, by the use of alternate or simplified calculational methods, or by the performance of a suitable testing program.
Contrary to the above, since August 7, 1985, the licensee failed to verify the adequacy of the design. Specifically, the licensee did not verify the design adequacy of support 1P42-H1080 because the associated structural evaluation failed to consider the impact of the rigid end connections of the W8 steel post and also failed to demonstrate acceptability of the W21 beam affected by the pipe support.
The licensee is still evaluating its planned corrective actions. However, the team determined that the continued non
-compliance does not present an immediate safety concern because the licensee performed an evaluation that reasonably concluded that the affected structures will remained operable
. Because this violation was of very
-low safety significance (Green) and was entered into the licensee's CAP as CR
-2017-08986 and CR
-2017-09043, this violation is being treated as an NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy. (NCV 05000440/2017008
-02; Inadequate Evaluation of Emergency Closed Cooling System Pipe Support)
.
.5 Operating Experience
a. Inspection Scope
The team reviewed three operating experience issues (samples) to ensure that generic concerns had been adequately evaluated and addressed by the licensee. The operating experience issues listed below were reviewed as part of this inspection:
IN 2007-01, "Recent Operating Experience Concerning Hydrostatic Barriers;"
IN 2015-01, "Degraded Ability To Mitigate Flooding Events;"
and Part 21 No. 2013 00, "Wedge Pin Failure of an Anchor/Darling Double
-Disc Gate Valve at Browns Ferry Nuclear Plant U1."
b. Findings
No findings were identified.
18
.6 Operating Procedure Accident Scenarios
a. Inspection Scope
The team performed a detailed reviewed of the procedures listed below. The procedures were compared to UFSAR, design assumptions, and training materials to assess their consistency
. The following operating procedures were reviewed in detail:
Emergency Operating Procedure (EOP)-01A Chart, "Level Power Control," Revision H; EOP-02 Chart, "Primary Containment Control," Revision F; EOP-SPI 3.2, "Suppression Pool Makeup," Revision 1; EOP-SPI 6.4, "HPCS Injection," Revision 2; EOP-SPI 6.6, "RCIC Injection and Pressure Control," Revision 3; ONI-R10-1, "Loss of AC Power," Revision A; ONI-R10-2, "Station Blackout," Revision B; ONI-SPI C-3, "CST Transfer to Suppression Pool," Revision 4; ONI-SPI C-7, "Division 3 to Division 2 480 Volt Crosstie," Revision 5; ONI-SPI D-1, "Maintaining System Availability," Revision 5; ONI-SPI D-3, "Cross Tie Unit Batteries," Revision 5; ONI-ZZZ-1, "Tornado or High Winds," Revision 28; SOI-P45/P49, "Emergency Service Water and Screen Wash Systems," Revision 30; and SOI-P57, "Safety Related Instrument Air System," Revision 17. For the procedures listed, time dependent operator actions were reviewed for reasonableness. This review included walk downs of in
-plant actions with a licensed operator and the observations of licensed operator crews actions during the performance o f an SBO scenario in the station's simulator to assess operator knowledge level, adequacy of procedures, and availability of special equipment where required, and capability to perform time dependent operator actions within the required time. In addition, the team evaluated operations interfaces with other departments. The following operator actions were reviewed:
Emergency Service Water Pump Strainer(s) Manual Backwash during a LOOP
- Supply Outboard Main Steam Isolation Valve following a Loss of Instrument Air; Break Vacuum in the Emergency Service Water System during Internal Flooding; Restore Emergency AC Power following SBO recovery; Swap CST Suction from the CST to the Suppression Pool during a Tornado Warning; Operations of HPCS and RCIC during in EOP
-1 during Cold Weather Conditions; Transfer CST Water to Suppression Pool Directly during Cold Weather SBO; Dump the Upper Containment Pool into the Suppression Pool during an SBO; Power Containment Isolation Valves during an SBO; Cross-tie Unit Batteries during an SBO; Cross-tie Division II to Division III during an SBO; and Open Control Room Cabinets during an SBO.
b. Findings
(1) Failure to Verify the Capability to Manually Backwash the Emergency Service Water Strainer during Loss of Offsite Power
Introduction:
The team identified a finding of very
-low safety significance (Green) and an associated NCV of 10 CFR Part 50, Appendix B, Criterion III, "Design Control," for the failure to verify the capability to manually backwash the Emergency Service Water (ESW) strainer during a LOOP. Specifically, the licensee credited the capability to manually backwash the ESW strainers during a LOOP. However, the associated differential pressure alarm setpoint did not ensure sufficient time to complete this activity because the alarms were set at the same value as the design differential pressure value assumed by the hydraulic calculations.
Description
- The ESW system is equipped with strainers that need to be manually backwashed during a LOOP with high differential pressure. Specifically, Revision 12 of UFSAR Section 9.2.1, "Emergency Service Water System," stated
, "The emergency service water strainers are driven by nonsafety
-related motors from nonsafety
-related power supplies." In addition, it stated
, "Manual backwash will, therefore, be required after a LOOP.
" Plant procedure s direct operators to manually backwash the strainers if a high differential pressure alarm is received.
However, the team noted that the high differential pressure alarm setpoint value did not provide sufficient time to complete the manual backwash before clogging conditions adversely affect the ESW system flow. Specifically, the licensee estimated that it would take approximately 2 to 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> to manually backwash the strainers during an in
-field walk down of the backwash procedure that the team observed. In contrast, ESW Hydraulic Calculation P45
-057, "Emergency Service Water System Thermal Hydraulic Model," Revision 3, assumed a strainer differential pressure value that was equal to the alarm setpoint. Thus, the alarm setpoint did include any allowance for additional debris accumulation on the strainer while the manual backwash is completed.
The licensee captured the team's concerns in their CAP as CR
-2017-09033 on August 31, 2017. The immediate corrective action was to perform a past and current operability review that reasonably determined the ESW remained operable by crediting unused margin reserved for potential pump degradation. The proposed corrective actions to restore compliance was to revise the associated calculation and the alarm setpoint to ensure sufficient to perform the required manual actions during a LOOP.
Analysis:
The team determined that the failure to verify the capability to manually backwash the ESW strainer during LOOP was contrary to 10 CFR Part 50, Appendix B, Criterion III, "Design Control," and was a performance deficiency.
The performance 20 deficiency was determined to be more
-than-minor because it was associated with the Mitigating Systems cornerstone attribute of protection against external factors and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the performance deficiency did not assure the ESW capability to supply the required minimum flow to its supported components.
The team determined the finding could be evaluated using the SDP in accordance with IMC 0609, "Significance Determination Process," Attachment 0609.04, "Initial Characterization of Findings," issued on October 7, 2016. Because the finding impacted the Mitigating Systems cornerstone, the team screened the finding through IMC 0609, Appendix A, "The Significance Determination Process for Findings At-Power," issued on June 19, 2012, using Exhibit 2, "Mitigating Systems Screening Questions." The finding screened as of very
-low safety significance (Green) because it did not result in the loss of operability or functionality of mitigating systems. Specifically, the licensee performed a past and current operability review that reasonably determined the ESW remained operable by crediting unused margin reserved for potential pump degradation.
The team did not identify a cross
-cutting aspect associated with this finding because it was not confirmed to reflect current performance due to the age of the performance deficiency.
Specifically, the alarm setpoint was established more than 3 years ago.
Enforcement
- Title 10 CFR Part 50, Appendix B, Criterion I II, "Design Control," states, in part, that measures shall be established for verifying or checking the adequacy of design, such as by the performance of design reviews, by the use of alternate or simplified calculational methods, or by the performance of a suitable testing program.
Contrary to the above, as of August 31, 2017, the licensee failed to verify the design adequacy of ESW, a safety
-related system
. Specifically, the licensing basis credited the capability to manually backwash the ESW strainers during a LOOP. However, the associated differential pressure alarm setpoint did not ensure sufficient time to complete this activity because the alarms were set at the same value as the design differential pressure value assumed by the hydraulic calculations. The licensee is still evaluating its planned corrective actions. However, this issue does not present an immediate safety concern because the licensee performed a past and current operability review that reasonably determined the ESW had unused margin reserved for pump degradation that could be temporarily used to allow sufficient time to complete a manual backwash during a LOOP
. Because this violation was of very
-low safety significance (Green) and was entered into the licensee's CAP as CR
-2017-09033, this violation is being treated as an NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy.
-03, Failure to Verify the Capability to Manually Backwash the Emergency Service Water Strainer during Loss of Offsite Power
)
OTHER ACTIVITIES
4OA2 Identification and Resolution of Problems
.1 Review of
Items Entered Into the Corrective Action Program
a. Inspection Scope
The team reviewed a sample of problems identified by the licensee associated with the selected samples and that were entered into the CAP. The team reviewed these issues to verify an appropriate threshold for identifying issues and to evaluate the effectiveness of corrective actions related to design issues. In addition, corrective action documents written on issues identified during the inspection were reviewed to verify adequate problem identification and incorporation of the problem into the CAP. The specific corrective action documents sampled and reviewed by the team are listed in the attachment to this report.
The team also selected four issues identified during previous component design basis inspections to verify that the concern s were adequately evaluated and corrective actions were identified and implemented to resolve the concern, as necessary. The following issues were reviewed:
-04, "Inadequate Procedures for Controlling Flow into Reactor Vessel;"
-01, "Failure to Adequately Protect Safety
-Related Equipment from Internal Flooding;"
-02, "Inadequate Control Circuit Voltage Calculation for Safety-Related Contactors;" and NCV 05000440/2016007
-02, "Use of Unapproved Standard for Site Flooding Modification and Associated
Analysis.
"
b. Findings
No findings were identified
.
4OA6 Management Meetings
.1 Interim Meeting Summary
On September 1 4, 2017, the team presented the preliminary inspection results to Mr. D. Hamilton and other members of the licensee staff. The licensee acknowledged the issues presented. The team confirmed that several documents reviewed were considered proprietary and were handled in accordance with the NRC policy related to proprietary information. The team had outstanding questions that required additional review and a follow
-up exit meeting.
22
.2 Exit Meeting Summary
On November 22, 2017, the team presented the inspection results to Mr. N. Conicella and other members of the licensee staff. The licensee acknowledged the issues presented.
The team asked the licensee whether any materials examined during the inspection should be considered proprietary. Several documents reviewed by the team were considered proprietary information and were either returned to the licensee or handled in accordance with NRC policy on proprietary information.
ATTACHMENT:
SUPPLEMENTAL INFORMATION
SUPPLEMENTAL INFORMATION KEY POINTS OF CONTAC
T Licensee
- D. Hamilton, Vice President
- F. Payne, Plant General Manager
- N. Conicella, Regulatory Compliance Manager
- D. Reeves, Site Engineering Director
- L. Zerr, Regulatory Compliance Supervisor
- T. Kledzik, Regulatory Compliance Engineer
U.S. Nuclear Regulatory Commission
M. Jeffers
, Branch Chief
- N. Féliz Adorno, Senior Reactor Inspector
LIST OF ITEMS OPENED, CLOSED, AND DISCUS
SED Opened and Closed
-01 NCV Failure to Address the Susceptibility of the Condensate Storage Tank
Low Level Instrument Lines to Freeze (Section 1R21.3.b(1))
-02 NCV Inadequate Evaluation of Emergency Closed Cooling System Pipe Support
(Section1R21.4.b(1))
-03 NCV Failure to Verify the Capability to Manually Backwash the Emergency Service Water
Strainer during Loss of Offsite Power
(Section 1R21.6.b(2))
Discussed
None
LIST OF DOCUMENTS REVIEWED The following is a list of documents reviewed during the inspection. Inclusion on this list does not imply that the NRC inspectors reviewed the documents in their entirety, but rather, that selected sections of portions of the documents were evaluated as part of the overall
inspection effort. Inclusion of a document on this list does not imply NRC acceptance of the document or any part of it, unless this is stated in the body of the inspection report.
CALCULATIONS
Number Description or Title
Date or Revision PSTG-0001 PNPP Class 1E Power Distribution System Voltage Study
PRMV-0062 4.16 kV Degraded Voltage Instrumentation Loop Calculation
MISC-0017 Effect of Voltage and Frequency on Induction Motors 0 PRMV-0016 High Pressure Core Spray Motor 1E22C001 Protective Relays Setpoints
MISC-0017 Effect of Voltage and Frequency on Induction Motor Speed
PRMV-0008 U1 EH Bus Supply Breakers, Preferred and Alternate
PRMV-0014 Div 3 HPCS Diesel Generator (1E22S001)/EH1301 Protective Relaying Setpoints
SBO-007 A01 Loss of Heat Tracing
- CST/HPCS Instrument Line
E22-043 HPCS System Thermal
-Hydraulic Analysis
0P42-0111 Self-Weight Excitation Review of Hangers for Emergency Closed Cooling System
9, A-02 4:04.9.2 P57 Tank Anchor Bolt Design
EA0021 P57 Low Pressure Storage Tanks
P57-13 Required Air Volume and Leakage Acceptance Criteria for the Division 1 and 2 Safety Related Instrument Air (P57) System
1P57-101-#007 Calculation for Pipe Supports MK
-1P57-H1140 / H1141
2/05/1984 PRDC-0016 Division 3, 125 Vdc Load Evaluation, Voltage Drop, Battery/Charger Sizing Calculation
PRDC-0017 Hydrogen Gas Generation in Unit 1 & 2 Division 3 Battery Rooms 0 PSTG-0001 MCC Voltages for Control Circuits
PRDC-0002 Unit 1 Divisions 1, 2 and 3 125 Vdc System Coordination
E22-042 Division 3 Emergency Diesel Generator Jacket Water Heat Exchanger Performance Test
P45-T02 Non-Safety Related Setpoint Tolerances for Emergency
Service/ Standby Diesel generators Heat Exchangers Low Flow Alarm 1P45N0073A/B
SBO-007 Loss of Heat Tracing
- CST/HPCS Instrument Line
0, A-01 R45C04 Div 1, 2, & 3 Diesel Generator Fuel Oil Day Tank improved Technical Specification Volume Calculation
CALCULATIONS
Number Description or Title
Date or Revision E22-037 Design Basis Heat Load & Required ESW Flow for the HPCS DGJW HX 2 E22-041 Div 3 Emergency Diesel Generator Jacket Water Heat
Exchanger Performance Test Evaluation 8/27/03
E22-042 Division 3 Emergency Diesel Generator Jacket Water Heat Exchanger Performance Test
CALCULATIONS
Number Description or Title
Revision E22-029 SVI-E22-T2001 , HPCS Pump Performance Test Acceptance Criteria 7 E22-043 High Pressure Core Spray (HPCS) System Thermal
-Hydraulic Analysis
R45-009 Determine Fuel Oil Volume Required to Support Operation of Standby and HPCS Diesel Generators
P45-023 Emergency Service Water (ESW/P45) System Overpressure Analysis 3 R44-007 Starting Air Leakage Criteria for the Standby and HPCS EDGs Starting Air (R44) System
P45-057 ESW System Thermal Hydraulic Model
CORRECTIVE ACTION DOCUMENTS GENERATED DUE TO THE INSPECTION
Number Description or Title
Date CR-2017-08481 NRC ID DBI Inspection: Minor Discrepancy Identified in SRIA Training Material
08/15/2017 CR-2017-08504 NRC ID DBAI Inspection: Calculation Clarification Required
08/16/2017 CR-2017-08685 NRC ID DBAI Inspection: Question Regarding Contingency Actions During Cold Weather and CST Level Instrumentation
08/23/2017 CR-2017-08725 NRC ID DBI Inspection: Use of Unconservative Concrete Compressive Strength in P57 Anchor Bolt Design Calculation
08/23/2017 CR-2017-08767 NRC ID DBAI Inspection: Station Blackout Time Critical Operator Actions 08/24/2017 CR-2017-08918 NRC ID DBAI Inspection: Procedure Inadequacy Related to Having HPCS Aligned to the Suppression Pool during an SBO
08/29/2017 CR-2017-08920 NRC ID DBAI Inspection: ONI
-R10 Improvements needed for SBO Time Critical Operator Actions
08/29/2017 CR-2017-08923 NRC ID DBAI Inspection: NRC Observation Related to EDG Starting Air
08/29/2017
CORRECTIVE ACTION DOCUMENTS GENERATED DUE TO THE INSPECTION
Number Description or Title
Date CR-2017-08481 NRC ID DBI Inspection: Minor Discrepancy Identified in SRIA Training Material
08/15/2017 CR-2017-08504 NRC ID DBAI Inspection: Calculation Clarification Required
08/16/2017 CR-2017-08685 NRC ID DBAI Inspection: Question Regarding Contingency Actions During Cold Weather and CST Level Instrumentation
08/23/2017 CR-2017-08725 NRC ID DBI Inspection: Use of Unconservative Concrete Compressive Strength in P57 Anchor Bolt Design Calculation
08/23/2017 CR-2017-08930 NRC ID DBAI Inspection: Calculation SBO
-007 Conservatism and Degraded CST Instrumentation Line Insulation
08/29/2017 CR-2017-08981 NRC ID DBAI Inspection: Minimum Temperature Not Included in HX Test Instruction
08/30/2017 CR-2017-08986 NRC ID DBAI Inspection: Emergency Closed Cooling Pipe Support 1P42H1080 Calculation (0P42
-0111 Rev. 9, A
-02) Inadequacies
08/30/2017 CR-2017-08967 NRC ID DBAI Inspection: Timed Constrained Operator Actions Validation
08/30/2017 CR-2017-09005 NRC ID DBAI Inspection: HPCS Alignment During a Tornadoes Warning Effects on the SBO Analysis
08/31/2017 CR-2017-09006 NRC ID DBAI Inspection: The SBO Analysis Requires 150k Gallons of Water from the CST which Affects ONI
-R10 Requirements
08/31/2017 CR-2017-09033 NRC ID DBAI Inspection: ESW Discharge Strainer Differential Pressure Alarms are Equivalent to the Design Maximum Value
08/31/2017 CR-2017-09036 NRC ID DBAI Inspection: Minor Error in Calculation 4:04.09.002
08/31/2017 CR-2017-09043 NRC ID DBI Inspection: Inadequate Justification Provided in Calculation 0P42
-0111 A-02 Regarding Impact on the Attached Beam 08/31/2017 CORRECTIVE ACTION DOCUMENTS REVIEWED DURING THE INSPECTION
Number Description or Title
Date CR-2013-11377 NRC ID 2013 50.59: LTA 50.59 Evaluation 09
-01526 07/24/2013 CR-2013-11217 NRC ID 50.59 2013
- Deficiencies with 50.59 Evaluation
09-01526 07/22/2013 CR-2013-10798 NRC ID 50.59, LTA Controls and Evaluation for SVI
-G33-T9131 for Irradiated Fuel in Upper Pool Storage Rack
07/15/2013 CR-2013-03364 High Pressure Core Spray (HPCS) Pump Performance
03/07/2013 CR-2014-11711 Snapshot Self
-Assessment SN
-SA-2014-0498 - Perry HPCS Pump & Motor ECP Readiness
07/14/2014 CR-2012-12844 EMI Test Results Indicate Increase Emissions 08/12/2012 CR-2013-03461 10 CFR Part 21 Issued for Components Applicable to Perry
03/08/2013 CR-2013-06927 Transmittal of BWROG TP
-13-006 05/02/2013
CORRECTIVE ACTION DOCUMENTS REVIEWED DURING THE INSPECTION
Number Description or Title
Date CR-2017-06730 Updated Industry Guidance to Address Part 21 Issue with Anchor Darling Double Disc Gate Valves
06/20/2017 CR-2015-08036 PFA Needed for Site Flooding Issues
06/08/2015 CR-2015-0579 External Flooding during a Probable Maximum Flooding Event
05/12/2015 CR-2016-11864 NRC ID: Underdrain Manhole Covers Changed to Grating vs. Watertight Covers
10/04/2016 CR-2006-00817 NRC ID - CDBI, Affects Drywell Backpressure Not Addressed in Calculation P57
-13 02/17/2006 CR-2016-26104 Wrong ID Number/Barcode on DLR Label
08/02/2016 CR-2011-06107 CDBI 2011
- ESW Discharge Valve Uses Modified Acceptance Criteria when Determining Adequate Starting Voltage
11/30/2011 CR-2011-05495 NRC CDBI- PSTG-0030 Omission of Resistive Values
11/15/2011 CR-2011-06244 NRC CDBI 2011
- Potential Green Non
-Cited Violation
2/02/2011 CR-2012-01195 NRC CDBI NCV, Inadequate Control Circuit
Voltage Calculation for Safety
-Related Motor Starter Contactors
01/24/2012 CR-2011-06226 2011 CDBI
- Potential Green Non
-Cited Violation
2/02/2011 CR-2005-04296 NRC Published IN 05
-11 05/16/2005 CR-2005-05933 NRC Observation of Building Floor Plugs
08/01/2005 CR-2011-05217 Internal Flooding Calculation Assumptions for system Isolation Not Identified
11/10/2011 CR-2010-87582 Technical Basis for Div 3 Air Rec Inlet Ckv Vlv EC Testing Cannot Be Found
2/29/2010 CR-2015-14494 Excessive Analytical Uncertainty Associated with Test Data Obtained per PTI
-R46-P00001-B 10/23/2015 CR-2012-11858 Degraded Insulation on Piping in the CST Dike for Heat Trace
07/31/2012 CR-2015-02273 CST Level Transmitters Room Temp
- Monitoring Heat Trace Not Maintaining Proper Temperature
2/22/2015 CR-2011-05217 Internal Flooding Calculation Assumptions for System Isolation Not Identified
11/10/2011 CR-2011-06227 Reportability Requirements For Internal Flooding Calculation
JL-083 Issues (NCV)
2/12/2011 CR-2011-06237 Non-Cited Violation for Operator Actions Assumed in JL
-083 Not Translated into Procedures
2/12/2011 CR-2011-06530 8-Hour ENS Report Needed for Control Complex Flooding Calculation Issue
2/07/2011 CR-2012-01194 NRC CDBI NCV, Failure to Adequately Protect Safety Related Equipment from Internal Flooding
01/24/2012 CR-2015-08036 PFA Needed for Site flooding Issues
06/08/2015 CR-2015-14025 10CFR50.59 Review Committee Identified Concerns with 50.59 Eval 14-01234 10/16/2015
CORRECTIVE ACTION DOCUMENTS REVIEWED DURING THE INSPECTION
Number Description or Title
Date CR-2016-06744 2016 NRC Mod/ 50.59 Inspection: Evaluation 14
-01234 (PNPP External Flooding) Questions
05/13/2016 CR-2016-06882 2016 NRC Mod/ 50.59 Inspection: 50.59 Evaluation 14
-01234 Departure in Methodology Required Prior NRC Approval
05/18/2016 CR-2015-05079 External Flooding during a Probable Maximum Flooding Event (West Side of Plant)
04/12/2015 DRAWINGS Number Description or Title
Date or Revision 206-0010-00000-FF Main One Line Diagram 13.8kV & 4.16kV
FF 208-0218- 00006-S Back Up Fuel Oil Transfer Pump 1R45
-C002C S 206-0015-00000-FF Non Class 1E 13.8kV Start
-Up Bus L10 & L20
FF D-206-018 One Line Diagram Class 1E 4.16kV Bus EH13
Z 022-0010-00000 Environmental Conditions for Control Building
K 1190E21 1P57-A003B, SRIA Storage Tank, Sh 1, 2
MK-1P42-H1080 Pipe Support Drawing
B 215-0431-00501 Conduit Layout, Intermediate Building
- North - E
- L. 620'-6" YY D-513-016 Intermediate Building, Structural Steel Framing, El. 637',
639'-6", and 642'
C D-412-222-86-0602D, CUN 4805
Air Instrument Storage Tank Anchorage Details
09/25/1986 302-0271-00000 Piping System Diagram, Safety Related Instrument Air System
S MK-1P57-H1140 Pipe Support Drawing
MK-1P57-H1141 Pipe Support Drawing
2/31/1984 B-208-199 Elementary Diagram 1P57F0015A
N 206-0050-00000 One-line Diagram, Unit 1, Class 1E, Division 3 DC System
Z 256-0050-00000 One-line Diagram, Unit 2, Class 1E, Division 3 DC System
N 302-0358-00000 Div. 3 Diesel starting Air/ Air Dryer Diagram
G 10 CFR 50.59 DOCUMENTS (SCREENINGS/SAFETY EVALUATIONS)
Number Description or Title
Date or Revision ONI-ZZZ-1 50.59 Applicability
Review for CST
Suction Swap to SP for
Tornado/Tornado Warning 05/1993 ONI-ZZZ-1 Tornado or High Winds
06/30/1995
10 CFR 50.59 DOCUMENTS (SCREENINGS/SAFETY EVALUATIONS)
Number Description or Title
Date or Revision 14-01322 Screening, Installation of Spent Fuel Pool Level Instrumentation for Beyond Design Basis External Events
MISCELLANEOUS
Number Description or Title
Date or Revision E22B SHR 2016
-3 System - E22B - High Pressure Core Spray Diesel Components
2/02/2017 OE-2012-1550 NRC Information Notices, IN12
-17 09/17/2012 OT-Combined-P57 Safety Related Instrument Air System (training material)
Qualification Report 108025 Rosemont Pressure Transmitter
D PRS-1700 Technical Requirements for Seismic analysis, Testing and Documentation of Mechanical and Electrical Equipment
System P57
Maintenance Rule System Basis Document
Engineering Report 84-02 Seismic Qualification Report (for valve 1P57
-F015B) 03/05/1984 Report WR 83
-27 Wyle Laboratories Report
- Qualification of Five Motor Operated Valve Assemblies
06/21/1983 600661784
EER - Evaluate Acceptable Seat Leakage Criteria for 1E22F0538A/B
01/14/2011 N/A Test Protocol
- HPCS Diesel Generator Jacket Water Heat Exchangers
06/11/2012 OE-2015-0025-3 IN15-01 Evaluation, Degraded Ability to Mitigate Flooding Events 01/16/2015 MODIFICATIONS
Number Description or Title
Revision ECP 12-0835-000 Installation of SFP Instrumentation
ECP 00-1120 Part / Component Equivalent Replacement Package
- Torque Switch for Limitorque SMB
-000 Actuators, Clamp Style
ECP 14-0228-001 New EDG Fuel Oil Level Instruments
ECP 09-0573 Emergency Service Water "C" Pump Refurbishment
ECP 11-0755 Place Sand Bags in Control Complex at Door IB
-103 0
PROCEDURES
Number Description or Title
Revision ARI-H13-P601-0016 DIV 3 Diesel Gen & HPCS
ONI-E12-1 Inadvertent Initiation of ECCS/RCIC
SOI-R44/E22B Division 3 Diesel Generator Starting Air System
SOI-R44 Division 1 and 2 Diesel Generator Starting Air System
ONI-SPI C-2 HPCS System Alignment
SOI-E22A High Pressure Core Spray System
ARI-E22-P001 HPCS Diesel Generator Control Panel
ARI-H13-P601-0016 DIV 3 Diesel Gen & HPCS
ONI-R10 Loss of AC Power
ONI-SPI C-5 Division 3 EDG Restoration
SOI-E22B Division 3 Diesel Generator
SVI-R22-T5069 Division 1 4.16 kV Bus EH11 Degraded Voltage Channel Functional Test
SVI-R22-T5070 Division 2 4.16 kV Bus EH12 Degraded Voltage Channel Functional Test
SVI-R22-T5071 Division 34.16 kV Bus EH13Degraded Voltage Channel Functional Test
SVI-R22-T5072 Division 1 4 kV Bus EH11 Undervoltage/Degraded Voltage Channel Calibration and Logic System Functional Test
SVI-R22-T5073 Division 2 4 kV Bus EH12 Undervoltage/Degraded Voltage Channel Calibration and Logic System Functional Test
SVI-R22-T5074 Division 3 4 kV Bus EH13 Undervoltage/Degraded Voltage Channel Calibration and Logic System Functional Test
NOP-OP-1013 Control of Time Critical Operator Actions
ARI-H13-P601-0019 SRV's Outboard Isolation Valves and Main Steam
SOI-P57 Safety Related Instrument Air Syste
m 17 EOP Bases
Emergency Operating Procedure Bases
EOP-02 Primary Containment Control
EOP-03 Secondary Containment Control
EOP-04 Emergency Depressurization
ARI-H13-P877-002 Division 2 Power
ARI-H51-P054B Division 2 Diesel Engine Control Panel
SOI-M43 Diesel Generator Building Ventilation System
SOI-R45 Division 1 and Division 2 Generator Fuel Oil System
ARI-E22-P001 HPCS Diesel Generator Control Panel
ONI-R10-2 Station Blackout B
PROCEDURES
Number Description or Title
Revision ONI-R10-1 Loss of AC Power Flow Chart
A ONI-SPI-C-5 Division 3 EDG Restoration
SOI-R42 Division 3 DC Distribution
ONI-SPI-C-3 CST Transfer to Suppression
NOP-OP-1002 Conduct of Operations
SOI-P45/P49 Emergency Service Water and Screen Wash Systems
ONI-SPI-D-1 Maintaining System Availability
ONI-SPI-D-3 Cross-Tying Unit 1 and 2 Batteries
ONI-SPI-D-9 Makeup Water Sources
SVI-P57-T2001 Safety-Related Instrument Air MOV Operability Test
SVI-P57-T2003 1P57 F015A and 1P57 F020A Remote Shutdown
Position Indication Verification
SVI-R10-T5228 On-Site Power Distribution System Verification
ISI-E22-T1201-3 HPCS Standby Diesel Generator Starting Air System Inservice Pressure Test Class 3
ISI-R44-T1200-3 Standby Diesel Generator Starting Air System Inservice Pressure Test Class 3
PTI-E22-P0007 HPCS Diesel Generator Jacket Water Heat
Exchanger Performance Testing
SVI-E22-T2001 HPCS Pump and Valve Operability Test
SVI-R45-T2001 Division 1 Diesel Generator
Fuel Oil Transfer Pump and
Valve and Starting Air Check Valve Operability Test
SVI-R45-T2002 Division 2 Diesel Generator Fuel Oil Transfer Pump and
Valve and Starting Air Check Valve Operability Test
SVI-R45-T2003 Division 3 Diesel Generator Fuel Oil Transfer Pump and Valve and Starting Air Check Valve Operability Test
SVI-E22-T1183 HPCS Valve Lineup Verification and System Venting
SURVEILLANCES (COMPLETED) Number Description or Title
Date PY-ISI-P57T1200-2 Safety Related Instrument Air (SRAI) System Inservice Pressure Test
-Class 2 03/27/2017 PY-ISI-P57T1201-3 Safety Related Instrument Air (SRAI) System Inservice Pressure Test
-Class 3 03/13/2017 PY-ISI-P57T2001-1 Safety Related Instrument Air Motor Operated Valve Operability Test
04/19/2017 PY-ISI-P57T9116 Safety Related Instrument Air (SRAI) System Inservice Pressure Test
-Class 2 03/20/2017 PY-ISI-P57T2001 2
Safety Related Instrument Air Motor Operated Valve Operability Test (PI)
03/12/2017
SURVEILLANCES (COMPLETED) Number Description or Title
Date ISI-E22-T1201-3 HPCS Standby Diesel Generator Starting Air System Inservice Pressure Test Class 3
05/12/2016 ISI-E22-T1201-3 HPCS Standby Diesel Generator Starting Air System Inservice Pressure Test Class 3 11/19/2012 ISI-R44-T1200-3 Standby Diesel Generator Starting Air System Inservice Pressure Test Class 3
11/19/2012 ISI-R44-T1200-3 Standby Diesel Generator Starting Air System Inservice Pressure Test Class 3
06/29/2015 PTI-E22-P0007 HPCS Diesel Generator Jacket Water Heat Exchanger Performance Testing
08/04/2008 PTI-E22-P0007 HPCS Diesel Generator Jacket Water Heat Exchanger Performance Testing
2/16/2010 PTI-E22-P0007 HPCS Diesel Generator Jacket Water Heat Exchanger Performance Testing
05/12/2015 SVI-E22-T2001 HPCS Pump and Valve Operability Test
2/06/2017 WORK DOCUMENTS
Number Description or Title
Date 200513404
Perform Static Test/Limitorque
Maintenance (PMI
-0030) 03/22/2015 200061492
Perform Static Test/Limitorque Maintenance (PMI
-0030) 03/15/2005 200680513
Perform Operability Test of 1P57F0015 A & B
04/19/2017 200279346
Month Performance Test of Unit 1, Division 3 Battery Capacity 08/05/2013 200600623
Month Service Test of Unit 1, Division 3 Battery Capacity
2/16/2016 200680607
Day Unit 1, Division 3 Battery Category B Limits, Terminal Corrosion and Electrolyte Temperature Check
05/11/2017 200660494
On-Site Power Distribution System Verification
06/11/2017 200061492
Perform Full PMI
-0030 on MOV 1P57F0015B
03/15/2005
LIST OF ACRONYMS USE
D CAP Corrective Action Program
CFR Code of Federal Regulations
CR Condition Report
CST Condensate Storage Tank
ECP Engineering Change Package
EDG Emergency Diesel Generator
EOP Emergency Operating Procedure
ESW Emergency Service Water
IMC Inspection Manual Chapter
IN Information Notice
LERF Large Early Release Frequency LOOP Loss of Off
-site Power
NCV Non-Cited Violation
NRC U.S. Nuclear Regulatory Commission
RCIC Reactor Core Isolation Cooling
SBO Station Blackout
SDP Significance Determination Process
SPAR Standardized Plant Analysis Risk
SRA Senior Reactor Analyst UFSAR Updated Final Safety Analysis Report