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| * August 11, 1994 Mr. J. Meade R. Anderson, P.G. | | * August 11, 1994 Mr. J. Meade R. Anderson, P.G. |
| Department of Environmental Quality Piedmont Water Regional Office P.O. Box 6030 Glen Allen, VA 23058 RE: PC# 94-3824 SURRY POWER- STATION UNDERGROUND OIL RELEASE* | | Department of Environmental Quality Piedmont Water Regional Office P.O. Box 6030 Glen Allen, VA 23058 RE: PC# 94-3824 SURRY POWER- STATION UNDERGROUND OIL RELEASE* |
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| Mr,. ~eade Anderson August 11, 1994 | | Mr,. ~eade Anderson August 11, 1994 |
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| | Page 2 i The fuel oil lines are encased together in concrete~ The leaking line has been abandoned and the EOG switched to a spare line; therefore, the station did not have to excavate around the line . |
| I Page 2 i The fuel oil lines are encased together in concrete~ The leaking line has been abandoned and the EOG switched to a spare line; therefore, the station did not have to excavate around the line .
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| . The only excavation required was for access to the line for testing. No petroleum contamination was apparent in the excavated soil. We know from existing wells on site that the depth to groundwater is approximately 17 feet. The underground fuel oil i lines are associated with two underground tanks, which, due to* | | . The only excavation required was for access to the line for testing. No petroleum contamination was apparent in the excavated soil. We know from existing wells on site that the depth to groundwater is approximately 17 feet. The underground fuel oil i lines are associated with two underground tanks, which, due to* |
| their emergency generator status, are exempt from the UST regulations. During the investigation of the line leak, *the st"ticn did ne:t enccuntar any frse product;.t!1.erefcre, no effort was made to measure or remove free product and there were no saf~ty or fire hazards requiring mitigation. | | their emergency generator status, are exempt from the UST regulations. During the investigation of the line leak, *the st"ticn did ne:t enccuntar any frse product;.t!1.erefcre, no effort was made to measure or remove free product and there were no saf~ty or fire hazards requiring mitigation. |
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| *Region II 101 Marietta st., NW Suite 2900 Atlanta, GA 30323 Re: Surry Units l & 2 Docket Nos. 50-280/50281 License Nos. DPR-32/DPR-37 Nuclear Regulatory Commission Document .Control Desk Washington, DC 20555 Re: Surry Units 1 & 2 Docket Nos. 50-280/50281 License Nos. DPR-32/DPR-37 Mr. M. w. Branch NRC Senior resident Inspector Surry Power Station | | *Region II 101 Marietta st., NW Suite 2900 Atlanta, GA 30323 Re: Surry Units l & 2 Docket Nos. 50-280/50281 License Nos. DPR-32/DPR-37 Nuclear Regulatory Commission Document .Control Desk Washington, DC 20555 Re: Surry Units 1 & 2 Docket Nos. 50-280/50281 License Nos. DPR-32/DPR-37 Mr. M. w. Branch NRC Senior resident Inspector Surry Power Station |
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| 'I-Enclosure 2 INITIAL ABATEMENT MEASURES REPORT CHECKLIST | | 'I-Enclosure 2 INITIAL ABATEMENT MEASURES REPORT CHECKLIST |
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| * Regulated substance removed from UST system 2- I Efforts | | * Regulated substance removed from UST system 2- I Efforts to mitigate fire and safety hazards |
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| to mitigate fire and safety hazards | |
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| I Efforts to measure for the presence of free product 7- 4 I Efforts to remove iree product z I I Measures taken. as part of lnltlal Abatement, to address contaminated ground water and sous; tank water and sludges,* and debris Q.e. tanks, piping, concrete) lncl_ude permits | | I Efforts to measure for the presence of free product 7- 4 I Efforts to remove iree product z I I Measures taken. as part of lnltlal Abatement, to address contaminated ground water and sous; tank water and sludges,* and debris Q.e. tanks, piping, concrete) lncl_ude permits |
Similar Documents at Surry |
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Category:NPDES NONCOMPLIANCE NOTIFICATION
MONTHYEARML18153B0411994-08-11011 August 1994 NPDES Noncompliance Rept,Consisting of Initial Abatement Rept for SPS Petroleum Release Pc# 94-3824:on 940509,found Oil Sheen in Discharge Canal.Leaking Oil Line Taken Out of Svc & Interior of Pipe Inspected W/Boroscope ML18153A9401994-05-11011 May 1994 NPDES Noncompliance Notification:On 940509,oil Sheen Observed in Plant Discharge Canal.Hydrostatic Testing of Supply Lines to EDG Indicates Existence of Leak in One Line. Leaking Suppl Line Isolated Until Corrections Can Be Made ML18153B4361993-12-27027 December 1993 Submits follow-up to Telephone Notification of Oil Discharge Rept 94-1332.On 931220,oil Found at Permanent Oil Boom in Discharge Canal ML18153C8441991-12-18018 December 1991 NPDES Noncompliance Notification:On 911126,discharges Made from Outfalls 141 (Waste Neutralization Sump 1A) & 171 (Waste Neutralization Sump 2B) W/O Performing Full Discharge Monitoring.Standing Order to Chemistry Dept Issues ML18153C7441991-09-16016 September 1991 Confirms 910911 Unusual Discharge During Final Stages of Dewatering of High Level Intake Screen Well to Allow for Maint Operations.Solids from Bottom of Well Were Pumped Over to Storm Drain Leading to Outfall 001 ML18153B7261989-05-10010 May 1989 NPDES Noncompliance Notification:In Apr 1989,plant Experienced Two NPDES Permit Exceptions Re Operation of New Ultraviolet Sewage Treatment Sys.Corrective Actions Will Continue to Include Supplemental Wasting of Uv Tubes ML18153B6761989-04-0303 April 1989 NPDES Noncompliance Notification:Oil Spills Observed in Discharge Canal.Floating Containment Booms,Used to Contain Any Oil Discharges Permanently Installed Across Canal.Nrc to Be Notified If Release Escape Discrete Containment Area ML18153B6081989-02-13013 February 1989 NPDES Noncompliance Notification:On 890208,small Oil Sheen Discovered in Upper End of Station Discharge Canal.Caused by Oil Collection Pan Beneath Crane Accidentally Tipped Over. Absorbent Boom Placed at Mouth of Storm Drain ML18153B6071989-02-10010 February 1989 NPDES Noncompliance Notification:On 890119,average Permit Limit for Fecal Coliforms Exceeded 200 mpn/100 Milliliter. Util Will Keep State Informed of Status of Corrective Actions ML18153B5791989-01-0404 January 1989 Informs That on 880102,oil Sheen in Upper End of Station Discharge Canal Discovered.Caused by Failure of Storm Drain Boom Which Allowed Runoff.Absorbent Pads Used to Clean Up & Storm Drain Boom Replaced ML18153B5671988-12-30030 December 1988 NPDES Noncompliance Notification:On 881222,discovered Small Sheen of Oil in Condenser Cooling Water Discharge Canal. Caused by Oil Boom Around West Yard Coming Apart & Releasing Small Amount of Oil.Absorbent Matl Used to Clean Up Oil ML18153B4781988-06-23023 June 1988 NPDES Noncompliance Notification:On 880619,station Security Personnel Reported Oil Sheen in Station Discharge Canal. Caused by Faulty Skimmer on Turbine Sump B.Spill Was Contained by Temporary Boom Placed in Discharge Canal ML18152A9941988-06-13013 June 1988 NPDES Noncompliance Notification:On 880609,oil Sheen in Station Discharge Canal Discovered.Caused by Heavy Rainfall Making 5-10 Gallons of Oil to Overflow Through Storm Drain to Discharge Canal.Spill Contained W/Absorbent Boom ML20205S5901986-06-0505 June 1986 NPDES Noncompliance Notification:On 860521,Package Boiler 'A' Blowdown Tank,Discharge 091,discovered Drained.No Effluent Sample Obtained.Caused by Improperly Seated Valve. Formal Work Request Submitted for Repair of Valve ML20197D3591986-05-0707 May 1986 Noncompliance Notification:On 860429,composite Sample of Effluent from Outfall 011 Revealed Biological Oxygen Demand of 6.75 mg/1,exceeding Monthly Average Limit.Corrective Actions Successful ML20197B6021986-05-0202 May 1986 NPDES Noncompliance Notification:On 860422,biological Oxygen Demand of Composite Effluent Sample Exceeded Permit Limits. Caused by Introduction of Foreign Substance.Max Air Input to Generation Tanks & Return Sludge Provided ML18149A0421986-02-0404 February 1986 NPDES Noncompliance Notification:On 860121,composite Sample of Effluent Taken from Outfall 011,sewage Treatment Plant. Analytical Results Revealed Biological Oxygen Demand in Excess of Limits.Caused by Input of Clean Domestic Water ML20136D2331985-11-0606 November 1985 NPDES Noncompliance Notification:On 851025,analysis of Grab Sample Taken from Outfall 081 (Turbine Sump) Revealed Oil & Grease Level of 32.7 Mg.Probably Caused by Water Transfer from Collection Pits.No Corrective Action Needed ML18143B6491985-10-0404 October 1985 NPDES Noncompliance Notification:Flow for Outfall 011 Sewage Treatment Plant Estimated for Sept Rather than Reflecting Recorded Results.On 850928,sample Taken from Outfall 002 Oil Tank Diked Area Discharge Exceeded Limits ML20137W7001985-09-25025 September 1985 NPDES Noncompliance Notification:On 850907,chlorine Residual at Outfall 011 at Sewage Treatment Plant Exceeded Effluent Limitations.Subsequent Test Results within Limitations.No Corrective Action Planned ML20137M8231985-09-0606 September 1985 NPDES Noncompliance Notification:On 850828,flow Recording Pen for Outfall 011 Sewage Treatment Plant Did Not Respond to Input Voltage.Caused by Malfunctioning Flow Integrator Part.Daily Estimate of Flow Continuing ML20137B5111985-08-13013 August 1985 NPDES Noncompliance Notification:On 850810,analysis of Grab Sample Taken from Outfall 002 (Gas Turbine Oil Tank Dike), Revealed Ph Less than Allowed 6.0 Std Units.Probably Caused by Rainwater.No Corrective Actions Planned ML20133H2391985-07-31031 July 1985 NPDES Noncompliance Notification:On 850719,flow Recording Pen for Outfall 011 (Sewage Treatment Plant) Did Not Respond to Input Voltage.Caused by Malfunctioning Flow Integrator Parts.Parts Ordered & Nonrecording Meter Used ML20128L9121985-07-12012 July 1985 Supplemental NPDES Noncompliance Notification:On 850710, Review of June 1985 Discharge Monitoring Rept for Outfall 002 Revealed Excessive Total Suspended Solid Levels. Rainwater in Dike Will Be Retained for Longer Period ML20128L2451985-07-0909 July 1985 NPDES Noncompliance Notification:During June 1985,required Sampling of Process Stream 121 (Boron Recovery Sys),Not Taken,In Spite of 850601-03 Releases.Failure to Obtain Sample Discussed W/Personnel ML18142A4801985-06-17017 June 1985 NPDES Noncompliance Notification:On 850613,grab Sample from Outfall 002,gas Turbine Oil Tank Dike,Registered Ph of 5.7, Lower than 6.0 Ph Allowed by Permit.Probably Caused by Acid Rain,As Oil Spill from Tank Never Occurred ML20127D0331985-06-12012 June 1985 NPDES Noncompliance Notification:On 850610,max Permit Limit of 20 Mg/L Exceeded.Grab Sample Revealed Oil & Grease Content of 57.4 Mg/L.No Immediate Corrective Action Taken Due to Sample Taken After Discharge Completed ML20127D0461985-06-10010 June 1985 NPDES Noncompliance Notification:On 850605,oil Spilled in Facility Water Discharge Canal.Caused by Oil Entering Storm Drain from Nearby Equipment & Running Off During Heavy Rainfall.Spill Cleaned.Floating Boom Placed Around Drain ML20126C9511985-06-0303 June 1985 NPDES Noncompliance Notification:On 850529,oil Spill from Storm Drain Discovered.Caused by Surface Runoff Due to Rain. Oil Dispersed Before Cleanup Procedures Initiated ML18142A3881985-05-0202 May 1985 NPDES Noncompliance Notification:On 850430,total Suspended Solid Level Calculated from Sewage Treatment Plant Outfall 008 Effluent Exceeded Max Monthly Average Limit.Synthetic Seed Promoting Bacterial Action Will Be Used ML20115H3291985-04-0909 April 1985 NPDES Noncompliance Notification:On 850405,discovered Light Sheen of Oil 5x25 Ft in Station Discharge Canal.Caused by Failure of Oily Water Transfer Pump.Commercial Oil Sorbent Matl Used to Construct Containment & Pump Repaired ML18142A3371985-03-11011 March 1985 NPDES Noncompliance Notification:On 850305,06 & 07,excessive Ph Levels Discovered in Grab Samples from Outfalls 101 & 601.Corrected Jan 1985 NPDES Discharge Monitoring Rept for Outfall 601 Encl.W/O Encl ML20106G9391985-02-0101 February 1985 NPDES Noncompliance Notification:On 850130,100 Gallons of 0.0003% Hegatreat Solution Entered Turbine Basement Sump A. Procedure Stopped & Personnel Involved Instructed Not to Allow Release of Matl in Future ML20100P8211984-12-0303 December 1984 NPDES Noncompliance Notification:On 841130 & 1203,average Value of Total Suspended Solids & Average Value of BOD5 Exceeded Limit of 30 Mg/L,Respectively.Caused by Increased Hydraulic Load & Introduction of Foreign Substances ML18142A1281984-11-14014 November 1984 NPDES Noncompliance Notification:On 841107,4 H Composite Sample for Total Suspended Solids Exceeded Permit Limit. Caused by Increased Hydraulic Load at Peak Flow Times.Daily Wasting of Clarifier Sludge Undertaken ML18141A5031984-02-0909 February 1984 NPDES Noncompliance Notification:Updates Status of Chlorination Sys at Sewage Treatment Plant.Malfunctioning Gas Feed Sys Reported in 840201 Ltr Returned to Operation on 840203 ML18141A4941984-02-0303 February 1984 NPDES Noncompliance Notification:On 840201,discovered That Chlorine Gas Feed Sys Failed to Supply Chlorine to Effluent. Caused by False Rate Meter Reading Due to Water Pressure. Hypochlorite Addition Method Substituted ML18141A0791983-07-27027 July 1983 NPDES Noncompliance Notification:On 830715,grab Sample of Effluent from Sewage Treatment Plant Found Equal or Greater than 2,400 MPN/100 Ml.Caused by Foreign Substance in Sys. Foreign Substance Removed.No Adverse Impact Observed 1994-08-11
[Table view] Category:TEXT-ENVIRONMENTAL REPORTS
MONTHYEARML18151A2121998-12-31031 December 1998 Annual Radioactive Effluent Release Rept for Surry Power Station,Jan-Dec 1998. ML18152B7961997-12-31031 December 1997 1997 Annual Radiological Environ Operating Rept for 1997. W/980428 Ltr ML18153A2941997-12-31031 December 1997 Annual Radioactive Effluent Release Rept for Surry Power Station for 970101-1231. ML18153A1331996-12-31031 December 1996 1996 Annual Radiological Environ Operating Rept. W/970430 Ltr ML18151A2641996-12-31031 December 1996 Annual Radioactive Effluent Release Rept for Surry Power Station. ML18151A1511995-12-31031 December 1995 Radiological Environ Operating Rept, Jan-Dec 1995. ML18151A2991995-12-31031 December 1995 Annual Radioactive Effluent Release Rept Surry Power Station (Jan-Dec 1995). W/960422 Ltr ML18151A7081995-07-31031 July 1995 Mixing & Dilution of Surry Nuclear Power Plant Cooling Water Discharge Into James River. ML18151A1501994-12-31031 December 1994 Radiological Environ Monitoring Program Jan-Dec 1994. W/950427 Ltr ML18151A2951994-12-31031 December 1994 Annual Radioactive Effluent Release Rept Surry Power Station Jan-Dec 1994. W/950426 Ltr ML18153B0411994-08-11011 August 1994 NPDES Noncompliance Rept,Consisting of Initial Abatement Rept for SPS Petroleum Release Pc# 94-3824:on 940509,found Oil Sheen in Discharge Canal.Leaking Oil Line Taken Out of Svc & Interior of Pipe Inspected W/Boroscope ML18153A9401994-05-11011 May 1994 NPDES Noncompliance Notification:On 940509,oil Sheen Observed in Plant Discharge Canal.Hydrostatic Testing of Supply Lines to EDG Indicates Existence of Leak in One Line. Leaking Suppl Line Isolated Until Corrections Can Be Made ML18151A1481993-12-31031 December 1993 1993 Annual Radiological Environ Operating Rept. W/940425 Ltr ML18153B4361993-12-27027 December 1993 Submits follow-up to Telephone Notification of Oil Discharge Rept 94-1332.On 931220,oil Found at Permanent Oil Boom in Discharge Canal ML18150A4541992-12-31031 December 1992 Radiological Environ Monitoring Program,920101-1231. W/930427 Ltr ML18153D2811992-12-31031 December 1992 Recorded Annual Whole Body Exposure Rept for Surry Power Station,Units 1 & 2,for Period of 920101-1231. W/930326 Ltr ML18153C9131991-12-31031 December 1991 Semiannual Radioactive Effluent Release Rept for Jul-Dec 1991. ML18151A2921991-12-31031 December 1991 Annual Radiological Environ Operating Rept for 1991. W/ 920429 Ltr ML18153C9471991-12-31031 December 1991 Recorded Annual Whole Body Exposure Rept for Surry Power Station for Period Jan-Dec 1991. W/920327 Ltr ML18153C9161991-12-31031 December 1991 Semiannual Performance Data Rept for Jul-Dec 1991. W/ 920228 Ltr ML18153C8441991-12-18018 December 1991 NPDES Noncompliance Notification:On 911126,discharges Made from Outfalls 141 (Waste Neutralization Sump 1A) & 171 (Waste Neutralization Sump 2B) W/O Performing Full Discharge Monitoring.Standing Order to Chemistry Dept Issues ML18151A4991991-09-23023 September 1991 SPDES Permit VA0004090,issued to VEPCO ML18153C7441991-09-16016 September 1991 Confirms 910911 Unusual Discharge During Final Stages of Dewatering of High Level Intake Screen Well to Allow for Maint Operations.Solids from Bottom of Well Were Pumped Over to Storm Drain Leading to Outfall 001 ML18153C5551990-12-31031 December 1990 Semiannual Radioactive Effluent Release Rept for Jul-Dec 1990. W/910228 Ltr ML18151A3411990-12-31031 December 1990 1990 Annual Radiological Environ Operating Rept. W/910428 Ltr ML18153C5661990-12-31031 December 1990 Recorded Annual Whole Body Exposure Rept,Surry Station Isfsi,For 1990. W/910311 Ltr ML18153C1781989-12-31031 December 1989 Recorded Annual Whole Body Exposure Rept for 1989. W/900330 Ltr ML18153C1681989-12-31031 December 1989 Annual Whole Body Exposure Rept for 1989. W/900330 Ltr ML18151A4261989-12-31031 December 1989 1989 Radiological Environ Monitoring Program Rept. W/900430 Ltr ML18152A5251989-12-31031 December 1989 Reissued Semiannual Radioactive Effluent Release Rept, Jul-Dec 1989. ML18153B7261989-05-10010 May 1989 NPDES Noncompliance Notification:In Apr 1989,plant Experienced Two NPDES Permit Exceptions Re Operation of New Ultraviolet Sewage Treatment Sys.Corrective Actions Will Continue to Include Supplemental Wasting of Uv Tubes ML18153B6761989-04-0303 April 1989 NPDES Noncompliance Notification:Oil Spills Observed in Discharge Canal.Floating Containment Booms,Used to Contain Any Oil Discharges Permanently Installed Across Canal.Nrc to Be Notified If Release Escape Discrete Containment Area ML18153B6081989-02-13013 February 1989 NPDES Noncompliance Notification:On 890208,small Oil Sheen Discovered in Upper End of Station Discharge Canal.Caused by Oil Collection Pan Beneath Crane Accidentally Tipped Over. Absorbent Boom Placed at Mouth of Storm Drain ML18153B6071989-02-10010 February 1989 NPDES Noncompliance Notification:On 890119,average Permit Limit for Fecal Coliforms Exceeded 200 mpn/100 Milliliter. Util Will Keep State Informed of Status of Corrective Actions ML18153B5791989-01-0404 January 1989 Informs That on 880102,oil Sheen in Upper End of Station Discharge Canal Discovered.Caused by Failure of Storm Drain Boom Which Allowed Runoff.Absorbent Pads Used to Clean Up & Storm Drain Boom Replaced ML18151A4911988-12-31031 December 1988 Radiological Environ Monitoring Program for 1988. ML18153B6721988-12-31031 December 1988 Recorded Annual Whole Body Exposure Rept for 1988. W/890331 Ltr ML18152A0221988-12-31031 December 1988 Semiannual Radioactive Effluent Release Rept,Jul-Dec 1988. W/890302 Ltr ML18153B5671988-12-30030 December 1988 NPDES Noncompliance Notification:On 881222,discovered Small Sheen of Oil in Condenser Cooling Water Discharge Canal. Caused by Oil Boom Around West Yard Coming Apart & Releasing Small Amount of Oil.Absorbent Matl Used to Clean Up Oil ML18153B5011988-06-30030 June 1988 Semiannual Radioactive Effluent Release Rept,Jan-June 1988. W/880829 Ltr ML18153B4781988-06-23023 June 1988 NPDES Noncompliance Notification:On 880619,station Security Personnel Reported Oil Sheen in Station Discharge Canal. Caused by Faulty Skimmer on Turbine Sump B.Spill Was Contained by Temporary Boom Placed in Discharge Canal ML18152A9941988-06-13013 June 1988 NPDES Noncompliance Notification:On 880609,oil Sheen in Station Discharge Canal Discovered.Caused by Heavy Rainfall Making 5-10 Gallons of Oil to Overflow Through Storm Drain to Discharge Canal.Spill Contained W/Absorbent Boom ML18151A5361987-12-31031 December 1987 Radiological Environ Monitoring Program for 1987. ML18152A7641987-12-31031 December 1987 Annual Whole Body Exposure Rept for CY87. W/880223 Ltr ML18152A7701987-12-31031 December 1987 Semiannual Radioactive Effluent Release Rept,Jul-Dec 1987. W/880229 Ltr ML18151A0371987-06-30030 June 1987 Semiannual Radioactive Effluent Release Rept,Surry Power Station,Jan-June 1987. W/870831 Ltr ML20212H3641986-12-31031 December 1986 Semiannual Radioactive Effluent Release Rept,Surry Power Station,(Jul-Dec 1986) ML18150A0721986-12-31031 December 1986 Radiological Environ Monitoring Program,1986. W/870430 Ltr ML20215L8761986-09-30030 September 1986 TMI Aquatic Study Monthly Rept for Sept 1986 ML20205S5901986-06-0505 June 1986 NPDES Noncompliance Notification:On 860521,Package Boiler 'A' Blowdown Tank,Discharge 091,discovered Drained.No Effluent Sample Obtained.Caused by Improperly Seated Valve. Formal Work Request Submitted for Repair of Valve 1998-12-31
[Table view] |
Text
- August 11, 1994 Mr. J. Meade R. Anderson, P.G.
Department of Environmental Quality Piedmont Water Regional Office P.O. Box 6030 Glen Allen, VA 23058 RE: PC# 94-3824 SURRY POWER- STATION UNDERGROUND OIL RELEASE*
INITIAL ABATEMENT MEASURES REPORT De~= ........
.i,¥.a..,,.. * ,.. ... ~---.-----*
.£".Ll.,l"'""f.;..!- g--,,,1.,;..
The following is the Initial Abatement Report.for the Surry Power Station Petroleum Release, PC# 94-3824. The report was initially .
due June 13, 1994; however, we requested and received an extension until August .15*,- 1994. The Initial Abatement Measures Checklist is attached.
On May 9, 1994, station personnel noticed a fuel oil odor near the laundry storm drains *.. Personnel then checked the discharge canal and found an oil sheen in.the canal .. Operations dispatched a crew to respond to the oil in the discharge canal. The response team placed an oil containment boom at the west end. 0f the canal which, in conjunction with the existing boom, .contained all but a small amount of the oil. Personnel then accomplished cleanup using sorbent pads and "socks".
Station.personnel inspected all pipes and storm water conveyances leading to the discha~ge canal. No further discharge of oil was found nor was there*any evidence of additional oil.in any discharge route from the station. *
- Just prior to the discovery of the oil in the canal, the station had conducted a scheduled test run of an emergency diesel generator (EOG). Subsequent hydrostatic testing of the supply lines to the EOG indicated the existence of a leak. We believe that fuel oil leaked from the EOG supply lines and then made its way to the storm.
drain either directly or via the sand sump. . The sand sump is a dewatering sump used to lower the groundwater. level near the foundations of the plant buildings. The sump discharges to the storm drain where personnel noticed the fuel oil odor.
During the past few months, the station has been investigating the fuel oil line leak *. The leaking fuel oil line has been taken out of service. The interior of the pipe has been inspected with a boroscope, which allows personnel to view the inside surf ace of the pipe. Additionally, the station has pressure tested incremental lengths of the pipe in order to determine the exact location of the leak. The mechanism of failure has not yet been characteri*zed and the station is still attempting to determine the cause of the leak.
-~-- -- --- ----------
C40R?60?~9 04QR1~ /./~ f:;
~nR--~DOtK OSuOo~so S PDR JP '\1
Mr,. ~eade Anderson August 11, 1994
Page 2 i The fuel oil lines are encased together in concrete~ The leaking line has been abandoned and the EOG switched to a spare line; therefore, the station did not have to excavate around the line .
. The only excavation required was for access to the line for testing. No petroleum contamination was apparent in the excavated soil. We know from existing wells on site that the depth to groundwater is approximately 17 feet. The underground fuel oil i lines are associated with two underground tanks, which, due to*
their emergency generator status, are exempt from the UST regulations. During the investigation of the line leak, *the st"ticn did ne:t enccuntar any frse product;.t!1.erefcre, no effort was made to measure or remove free product and there were no saf~ty or fire hazards requiring mitigation.
Following the installation of monitoring wells and a study to determine the extent of oil in the subsurface, we will submit a Site Characterization Report.
Please contact Wes Sprouse at 273-3552 if you have any questions.
Sincerely, B. M. Marshall, P.E.
Manager, Water Quality cc:* u. s. Nuclear Regulatory Commission
- Region II 101 Marietta st., NW Suite 2900 Atlanta, GA 30323 Re: Surry Units l & 2 Docket Nos. 50-280/50281 License Nos. DPR-32/DPR-37 Nuclear Regulatory Commission Document .Control Desk Washington, DC 20555 Re: Surry Units 1 & 2 Docket Nos. 50-280/50281 License Nos. DPR-32/DPR-37 Mr. M. w. Branch NRC Senior resident Inspector Surry Power Station
~
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'I-Enclosure 2 INITIAL ABATEMENT MEASURES REPORT CHECKLIST
- Site: $0cz.,iy ~"':'en..* <;."tAr,orJ PC# q4 *-3E.J.Lf Region ?;~~Mo~*,
The following checklist must be filled out by the Responsible Party (RP) and/or the RP's Conswtant anct Included In the Initial Abatement Report. Indicate on the chackllst the page and HCtlon numbe wh.,. each Item 18 addressed In the attached repo,L Also Indicate on the checkllst the section and page number where Justification Is given for items omitted from the attached report., The contents of the report should reflect and be commensurate with the nature of the release, degree of contamination a~ complexlty of the site Investigation.
- 1. RELEASE INVESTIGATION AND CONFIRMATION STEPS
°l)ARll,j!'.,2.A ~t(
Page; / .&Hele~ .
_.......__ / :l. Evidence for suspecting a release has occurred*
.___ / 't -'~-- *Monitoring result., from releea detection used Results of tank/fine tightness test I s Actions taken to repalr,-replace; upgrade UST- *
- 2. SITE CHECK
..---.I_. . . . I _...'f__ Measures taken to Identify the source of release 2.. , __ , _ Depth to ground water
.:L / _____ Description and Justification of sampllng
__2.._._ I J types (ground water, sol) .
_ _2....._*_ / > locations Qnclude site map)
_ _2-._ / parameters, EPA methods, units, and detection llmlts
- 3. INITIAL ABATEMENT MEASURES
/ i .
f , */ 5 Release Inspection resuts and measures taken to prevent further migration of contaminates Into soDs and ground water
- JJ A 2-.
I
- Regulated substance removed from UST system 2- I Efforts to mitigate fire and safety hazards
,z.
I Efforts to measure for the presence of free product 7- 4 I Efforts to remove iree product z I I Measures taken. as part of lnltlal Abatement, to address contaminated ground water and sous; tank water and sludges,* and debris Q.e. tanks, piping, concrete) lncl_ude permits
/- I lnltlal Abatement M~res Report submitted within 20 days of release confirmation or*
extension granted FOR OFFICE USE ONLY COMMENTS:~---------------------------
- D E F I C I E N C I E S ; _ : - - - - - - - - - - - - - - - - - - - - - - - - - -
REVIEWED BY:,_.. _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ DATE: _ _ _ _ _ _ _ _ __