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 Issue dateTitleTopic
ML18153B04111 August 1994NPDES Noncompliance Rept,Consisting of Initial Abatement Rept for SPS Petroleum Release Pc# 94-3824:on 940509,found Oil Sheen in Discharge Canal.Leaking Oil Line Taken Out of Svc & Interior of Pipe Inspected W/BoroscopeHydrostatic
ML18153A94011 May 1994NPDES Noncompliance Notification:On 940509,oil Sheen Observed in Plant Discharge Canal.Hydrostatic Testing of Supply Lines to EDG Indicates Existence of Leak in One Line. Leaking Suppl Line Isolated Until Corrections Can Be MadeTime of Discovery
Hydrostatic
ML18153B43627 December 1993Submits follow-up to Telephone Notification of Oil Discharge Rept 94-1332.On 931220,oil Found at Permanent Oil Boom in Discharge CanalTime of Discovery
ML18153C84418 December 1991NPDES Noncompliance Notification:On 911126,discharges Made from Outfalls 141 (Waste Neutralization Sump 1A) & 171 (Waste Neutralization Sump 2B) W/O Performing Full Discharge Monitoring.Standing Order to Chemistry Dept Issues
ML18153C74416 September 1991Confirms 910911 Unusual Discharge During Final Stages of Dewatering of High Level Intake Screen Well to Allow for Maint Operations.Solids from Bottom of Well Were Pumped Over to Storm Drain Leading to Outfall 001
ML18153B72610 May 1989NPDES Noncompliance Notification:In Apr 1989,plant Experienced Two NPDES Permit Exceptions Re Operation of New Ultraviolet Sewage Treatment Sys.Corrective Actions Will Continue to Include Supplemental Wasting of Uv Tubes
ML18153B6763 April 1989NPDES Noncompliance Notification:Oil Spills Observed in Discharge Canal.Floating Containment Booms,Used to Contain Any Oil Discharges Permanently Installed Across Canal.Nrc to Be Notified If Release Escape Discrete Containment Area
ML18153B60813 February 1989NPDES Noncompliance Notification:On 890208,small Oil Sheen Discovered in Upper End of Station Discharge Canal.Caused by Oil Collection Pan Beneath Crane Accidentally Tipped Over. Absorbent Boom Placed at Mouth of Storm Drain
ML18153B60710 February 1989NPDES Noncompliance Notification:On 890119,average Permit Limit for Fecal Coliforms Exceeded 200 mpn/100 Milliliter. Util Will Keep State Informed of Status of Corrective Actions
ML18153B5794 January 1989Informs That on 880102,oil Sheen in Upper End of Station Discharge Canal Discovered.Caused by Failure of Storm Drain Boom Which Allowed Runoff.Absorbent Pads Used to Clean Up & Storm Drain Boom Replaced
ML18153B56730 December 1988NPDES Noncompliance Notification:On 881222,discovered Small Sheen of Oil in Condenser Cooling Water Discharge Canal. Caused by Oil Boom Around West Yard Coming Apart & Releasing Small Amount of Oil.Absorbent Matl Used to Clean Up Oil
ML18153B47823 June 1988NPDES Noncompliance Notification:On 880619,station Security Personnel Reported Oil Sheen in Station Discharge Canal. Caused by Faulty Skimmer on Turbine Sump B.Spill Was Contained by Temporary Boom Placed in Discharge Canal
ML18152A99413 June 1988NPDES Noncompliance Notification:On 880609,oil Sheen in Station Discharge Canal Discovered.Caused by Heavy Rainfall Making 5-10 Gallons of Oil to Overflow Through Storm Drain to Discharge Canal.Spill Contained W/Absorbent Boom
ML20205S5905 June 1986NPDES Noncompliance Notification:On 860521,Package Boiler 'A' Blowdown Tank,Discharge 091,discovered Drained.No Effluent Sample Obtained.Caused by Improperly Seated Valve. Formal Work Request Submitted for Repair of Valve
ML20197D3597 May 1986Noncompliance Notification:On 860429,composite Sample of Effluent from Outfall 011 Revealed Biological Oxygen Demand of 6.75 mg/1,exceeding Monthly Average Limit.Corrective Actions Successful
ML20197B6022 May 1986NPDES Noncompliance Notification:On 860422,biological Oxygen Demand of Composite Effluent Sample Exceeded Permit Limits. Caused by Introduction of Foreign Substance.Max Air Input to Generation Tanks & Return Sludge Provided
ML18149A0424 February 1986NPDES Noncompliance Notification:On 860121,composite Sample of Effluent Taken from Outfall 011,sewage Treatment Plant. Analytical Results Revealed Biological Oxygen Demand in Excess of Limits.Caused by Input of Clean Domestic Water
ML20136D2336 November 1985NPDES Noncompliance Notification:On 851025,analysis of Grab Sample Taken from Outfall 081 (Turbine Sump) Revealed Oil & Grease Level of 32.7 Mg.Probably Caused by Water Transfer from Collection Pits.No Corrective Action NeededGrab sample
ML18143B6494 October 1985NPDES Noncompliance Notification:Flow for Outfall 011 Sewage Treatment Plant Estimated for Sept Rather than Reflecting Recorded Results.On 850928,sample Taken from Outfall 002 Oil Tank Diked Area Discharge Exceeded Limits
ML20137W70025 September 1985NPDES Noncompliance Notification:On 850907,chlorine Residual at Outfall 011 at Sewage Treatment Plant Exceeded Effluent Limitations.Subsequent Test Results within Limitations.No Corrective Action Planned
ML20137M8236 September 1985NPDES Noncompliance Notification:On 850828,flow Recording Pen for Outfall 011 Sewage Treatment Plant Did Not Respond to Input Voltage.Caused by Malfunctioning Flow Integrator Part.Daily Estimate of Flow Continuing
ML20137B51113 August 1985NPDES Noncompliance Notification:On 850810,analysis of Grab Sample Taken from Outfall 002 (Gas Turbine Oil Tank Dike), Revealed Ph Less than Allowed 6.0 Std Units.Probably Caused by Rainwater.No Corrective Actions PlannedGrab sample
ML20133H23931 July 1985NPDES Noncompliance Notification:On 850719,flow Recording Pen for Outfall 011 (Sewage Treatment Plant) Did Not Respond to Input Voltage.Caused by Malfunctioning Flow Integrator Parts.Parts Ordered & Nonrecording Meter Used
ML20128L91212 July 1985Supplemental NPDES Noncompliance Notification:On 850710, Review of June 1985 Discharge Monitoring Rept for Outfall 002 Revealed Excessive Total Suspended Solid Levels. Rainwater in Dike Will Be Retained for Longer Period
ML20128L2459 July 1985NPDES Noncompliance Notification:During June 1985,required Sampling of Process Stream 121 (Boron Recovery Sys),Not Taken,In Spite of 850601-03 Releases.Failure to Obtain Sample Discussed W/Personnel
ML18142A48017 June 1985NPDES Noncompliance Notification:On 850613,grab Sample from Outfall 002,gas Turbine Oil Tank Dike,Registered Ph of 5.7, Lower than 6.0 Ph Allowed by Permit.Probably Caused by Acid Rain,As Oil Spill from Tank Never OccurredGrab sample
ML20127D03312 June 1985NPDES Noncompliance Notification:On 850610,max Permit Limit of 20 Mg/L Exceeded.Grab Sample Revealed Oil & Grease Content of 57.4 Mg/L.No Immediate Corrective Action Taken Due to Sample Taken After Discharge CompletedGrab sample
ML20127D04610 June 1985NPDES Noncompliance Notification:On 850605,oil Spilled in Facility Water Discharge Canal.Caused by Oil Entering Storm Drain from Nearby Equipment & Running Off During Heavy Rainfall.Spill Cleaned.Floating Boom Placed Around Drain
ML20126C9513 June 1985NPDES Noncompliance Notification:On 850529,oil Spill from Storm Drain Discovered.Caused by Surface Runoff Due to Rain. Oil Dispersed Before Cleanup Procedures Initiated
ML18142A3882 May 1985NPDES Noncompliance Notification:On 850430,total Suspended Solid Level Calculated from Sewage Treatment Plant Outfall 008 Effluent Exceeded Max Monthly Average Limit.Synthetic Seed Promoting Bacterial Action Will Be Used
ML20115H3299 April 1985NPDES Noncompliance Notification:On 850405,discovered Light Sheen of Oil 5x25 Ft in Station Discharge Canal.Caused by Failure of Oily Water Transfer Pump.Commercial Oil Sorbent Matl Used to Construct Containment & Pump Repaired
ML18142A33711 March 1985NPDES Noncompliance Notification:On 850305,06 & 07,excessive Ph Levels Discovered in Grab Samples from Outfalls 101 & 601.Corrected Jan 1985 NPDES Discharge Monitoring Rept for Outfall 601 Encl.W/O EnclGrab sample
ML20106G9391 February 1985NPDES Noncompliance Notification:On 850130,100 Gallons of 0.0003% Hegatreat Solution Entered Turbine Basement Sump A. Procedure Stopped & Personnel Involved Instructed Not to Allow Release of Matl in Future
ML20100P8213 December 1984NPDES Noncompliance Notification:On 841130 & 1203,average Value of Total Suspended Solids & Average Value of BOD5 Exceeded Limit of 30 Mg/L,Respectively.Caused by Increased Hydraulic Load & Introduction of Foreign Substances
ML18142A12814 November 1984NPDES Noncompliance Notification:On 841107,4 H Composite Sample for Total Suspended Solids Exceeded Permit Limit. Caused by Increased Hydraulic Load at Peak Flow Times.Daily Wasting of Clarifier Sludge Undertaken
ML18141A5039 February 1984NPDES Noncompliance Notification:Updates Status of Chlorination Sys at Sewage Treatment Plant.Malfunctioning Gas Feed Sys Reported in 840201 Ltr Returned to Operation on 840203
ML18141A4943 February 1984NPDES Noncompliance Notification:On 840201,discovered That Chlorine Gas Feed Sys Failed to Supply Chlorine to Effluent. Caused by False Rate Meter Reading Due to Water Pressure. Hypochlorite Addition Method Substituted
ML18141A07927 July 1983NPDES Noncompliance Notification:On 830715,grab Sample of Effluent from Sewage Treatment Plant Found Equal or Greater than 2,400 MPN/100 Ml.Caused by Foreign Substance in Sys. Foreign Substance Removed.No Adverse Impact ObservedGrab sample