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| issue date = 09/22/1989
| issue date = 09/22/1989
| title = LER 89-009-00:on 890823,boric Acid Transfer Pump Seal Pot Found W/No Visible Level Resulting in No Flow Path to Rcs. Caused by Design of Boric Acid Transfer Pump Double Seals. Review Continuing for Alternate Seal design.W/890922 Ltr
| title = LER 89-009-00:on 890823,boric Acid Transfer Pump Seal Pot Found W/No Visible Level Resulting in No Flow Path to Rcs. Caused by Design of Boric Acid Transfer Pump Double Seals. Review Continuing for Alternate Seal design.W/890922 Ltr
| author name = GOLDBERG J H, HERRIN D W
| author name = Goldberg J, Herrin D
| author affiliation = FLORIDA POWER & LIGHT CO.
| author affiliation = FLORIDA POWER & LIGHT CO.
| addressee name =  
| addressee name =  
Line 16: Line 16:


=Text=
=Text=
{{#Wiki_filter:'CCE~mTED QBUTION DEMON+TION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)e ACCESSION NBR:8909270114 DOC.DATE: 89/09/22 NOTARIZED:
{{#Wiki_filter:'CCE~mTED                 QBUTION                               DEMON+TION             SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS) e ACCESSION NBR:8909270114                         DOC.DATE:   89/09/22     NOTARIZED: NO           DOCKET FACIL:50-251 Turkey Point Plant, Unit 4, Florida Power and Light                               C 05000251 AUTH. NAME           AUTHOR AFFILIATION HERRIN,D.W.           Florida         Power & Light Co.
NO DOCKET FACIL:50-251 Turkey Point Plant, Unit 4, Florida Power and Light C 05000251 AUTH.NAME AUTHOR AFFILIATION HERRIN,D.W.
GOLDBERG,J.H.         Florida         Power & Light Co.
Florida Power&Light Co.GOLDBERG,J.H.
RECIP.NAME           RECIPIENT AFFILIATION k
Florida Power&Light Co.RECIP.NAME RECIPIENT AFFILIATION k  


==SUBJECT:==
==SUBJECT:==
LER 89-009-00:on 890823,boric acid transfer pump seal pot found w/no visible level resulting in no flow path..W/8 ltr.DISTRIBUTION CODE-IE22T COPIES RECEIVED:LTR ENCL g SIZE: TITLE: 50.73/50.9 Licensee Event Report (LER), Incident'Rpt, etc.NOTES: RECIPIENT ID CODE/NAME PD2-2 LA EDISON,G INTERNAL ACRS MICHELSON ACRS WYLIE AEOD/DSP/TPAB DEDRO NRR/DEST/ESB 8D NRR/DEST/MEB 9H NRR/DEST/PSB 8D NRR/DEST/SGB 8D NRR/DLPQ/PEB 10.NRR D E RPB 10 RGN2 FILE 01 EXTERNAL: EG&G WILLIAMS,S LPDR NSIC MAYS,G NUDOCS FULL TXT COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 2 2 1 1 1 1 4 4 1 1 1 1 1 1 RECIPIENT ID CODE/NAME PD2-2 PD ACRS MOELLER AEOD/DOA AEOD/ROAB/DSP NRR/DEST/CEB 8H NRR/DEST/ICSB 7.NRR/DEST/MTB 9H NRR/DEST/RSB 8E NRR/DLPQ/HFB 10 NRR/DOEA/EAB 11 NUDOCS-ABSTRACT RES/DSIR/EIB L ST LOBBY WARD NRC PDR NSIC MURPHY,G.A COPIES LTTR ENCL 1 1 2 2 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1,1 1 1 1 1 1 1 1 1 1 1 NOXF TO ALL'%ZC6" RECIPIENTS'IZASE HELP US'IO REXQCB%@PTER QMIRCT THE DOCUMENI'GNTBOL DESK RXH Pl-37 (EXT.20079)m ELIMINAXB YOUR NAME PKH DISTEGBVX'ION.
LER   89-009-00:on 890823,boric acid                       transfer pump seal pot found w/no visible level resulting                         in no flow path..
LISTS HXR DOCUMENTS YOU DCK'T NEEDf FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 39 ENCL 39 P.O.Box14000, Juno Beach, FL 33408-0420 SEPTEMBER 2 2 1989 L-89-347 10 CFR 50.73 U.S.Nuclear Regulatory Commission Attn: Document Control Desk Washington, D.C.20555 Gentlemen:
W/8         ltr.
Re: Turkey Point Unit 4 Docket No.50-251 Reportable Event: 89-09 Date of Event: August 23, 1989 Boric Acid Transfer Pump Seal Pot Found With No Visible Level Resulting in No Flow Path From the Boric Acid Tank to Unit 4 Reactor Coolant S stem The attached Licensee Event Report is being submitted pursuant to the requirements of 10 CFR 50.73 to provide notification of the subject event.Very truly yours, J.H.Goldberg l Executive Vice President JHG/JRH/cm cc: Stewart D.Ebneter, Regional Administrator, Region II, USNRC Senior Resident Inspector, USNRC, Turkey Point Plant PDR 14 gyoy2 ADOC~0-0002Z1 PDt./i/(an FPL Group company
DISTRIBUTION CODE- IE22T COPIES RECEIVED:LTR TITLE: 50.73/50.9 Licensee Event Report (LER),
~0)l i',r, ,I NRC Form 355 I(cd')LICENSEE EVENT REPORT ILERI US.NUCLEAR AEOULATORY COMMISSION AppRDYED DMR No.31500101 EXPIRES: 5/31/55 FACILITY NAME (1)DOCKET NVMSKA (2)PA Turkey Point Unit 4 TITLE Iel I 1c rans er ump o 1 s1 e eye No Flow Path From Boric Acid Tank to Unit 4 Reactor Coolant System 02 51 1 OF p 3 ng 1n EVKNT DATE (5)LER NUMSEA (SI AEPOAT DATE (7)OTHER FACILITIES INVOLVED (SI MONTH DAY YEAR YEAR<cN SSOVSNTIAL tri5/ted~MONTH NVMSKR 4C NVMSSR DAY YEAR FACILITY NAMES DOCK ET NUM 5 5 R(SI 0 5 0 0 0 823 8 9 8 9 009 0 00 9 22 89 0 5 0 0 0 OPKAATINQ]MODE (SI POTTER LEVEL 1 P P II OI Qr~<%20A02()r I 20AOS(~l(1)(0 20AOS(e)II)(5)20.405(el Ill(QII 20405 le)(1)IN)20405(el(1)(c) 20.405(cl SOW(c)Ill 50.35(cl 12)50.73(e)12)Ill 50.73(cl(2)(5) 50.73(e)12)(llil 50.73(el l2)(Ic)50.73(e I (2)I x)50.73(e)12)
ENCL g  SIZE:
ITS)50.73(el(2)(vill)(AI 50.73(c)l2)(HIIIISI 50.73(el(2)(x)0 THE REQUIREMENTS OF 10 CFR g:/Chert one or more of the foll~no/(11 THIS REPORT IS SUSMITTKD PURSUANT T 73.710r)73.71(c)OTHEA/Specify/n Aptrrect Pe/owenPIn Teer HRCFonn 3654/NAME LICKNSEE CONTACT FOR THIS LER (12)Oennis W.Herrin, Regulation and Compliance Engineer TELEPHONE NVMSEA 305 24 6-6 731 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE OKSCAISED IN THIS REPORT (13)CAUSE SYSTEM COMPONENT MANVPAC TUAER CAUSE SYSTEM COMPONENT MANUFAC.TVRER EPORTABLE TO NPROS K~A..4 B C A SE AL 200 N'~~v'N'mN.: c.'.ac~%n)v jc~A%4 SUPPLEMENTAL REPORT EXPECTED (Ie)YES Ilf yet, complete EXPECTED SVSSIISSIOH DATE/NO ASSTAAOT ILlmit ro IFOO tpccet.I A.epproelmerely II/teen ring/ecpece lyf>>wr/tron llnnl (15)EXPECTED SV 5 MISS I ON DATE V5)MONTH OAY YEAR On August 23, 1989, at 1715, Unit 4 entered Technical Specification 3.0.1 for 33 minutes when the 4B Boric Acid Transfer Pump (BATP)was declared out of service.At the time of the event, the 4A BATP was out of service to repair a flange leak.At 1715, while making normal rounds, operations personnel discovered that the seal pot, which.pro-, vides seal cooling water to the 4B BATP, had no visible water level.Following the discovery, the 4B BATP seal pot was refilled and pump flow was verified.The seal pot level was observed, to remain stable.This was completed after 33 minutes, and Unit 4 exited Technical Speci-fication 3.0.1.The cause of this event is most likely attributable to the design of the BATP double seals.FPL believes that frequent pump starts and stops may cause axial shaft movement which results in separation of the inner seal faces.When the 4B BATP stopped automatic make-up to the Volume Control Tank at approximately 1700, FPL believes the inner seal faces temporarily"cocked", resulting in a drain of seal water into the pump casing.FPL engineering is continuing to re-view alternate seal designs for the BATPs which will not require quench water to the seal.NAC Form 355 (%531 NRC.For~388A I9>]l LICENS)4T REPORT (LER)TEXT CONTI U.S.NUCLEAR REQULATORY COMMISSION APPROVEO OMS NO.3)50M)04 EXPIRES: 8/3)/88 FACILITY NAME I)l Turkey Point Unit 4 OOCKET NUMBER Ill LER NUMSER I8)YEAR Q>g EEOUENTIAL sgrg~EVISIOH NUM\R'~: NUMSC/I PAGE (3)0 5 0 0 0 2 5 8 9 009-0 0 02 oF 0 3 Deseri tion of the Event On August 23, 1989, at 1715, Unit 4 entered Technical Specification 3.0.1 for 33 minutes when the 4B Boric Acid Transfer Pump (BATP)(EIIS:CA, Component:P) was declared out of service.Unit 4 was operating at 100 percent power with the-4A BATP out of service to repair a leak.At the time of this event, the 4B BATP was aligned to take suction from the C Boric Acid Tank (BAT)and dis-charge to the Unit 4 Charging Pumps, the 3A BATP was aligned to take suction from the A BAT and discharge to the Unit 3 Charging Pumps, and the 3B BATP was aligned to recirculate the B BAT.At 1715, the 4B BATP was declared out of service when Operations personnel making normal rounds discovered that the seal pot, which contains seal cool-ing water under Nitrogen (N2)pressure, had no visible water level.(These normal rounds are performed on a four hour interval.)
Incident'Rpt, etc.
Since the 4A BATP had previously been declared out of service, there was no flow path established from the BATs to the Unit 4 Reactor Coolant System (RCS).Technical Speci-fication 3.6.d requires that during power operation,"System piping, inter-locks and valves shall be operable to the extent of establishing one flow path from the boric acid tanks, and one flow path from the refueling water storage tank, to each Reactor Coolant System." Unit 4 entered Technical Specification
NOTES:
RECIPIENT                          COPIES            RECIPIENT         COPIES ID CODE/NAME                        LTTR ENCL        ID CODE/NAME     LTTR ENCL PD2-2 LA                               1    1        PD2-2 PD              1    1 EDISON,G                               1    1 INTERNAL ACRS MICHELSON                             1    1        ACRS MOELLER          2    2 ACRS WYLIE                             1    1        AEOD/DOA              1    1 AEOD/DSP/TPAB                           1    1        AEOD/ROAB/DSP        2    2 DEDRO                                   1    1        NRR/DEST/CEB 8H      1    1 NRR/DEST/ESB     8D                   1    1        NRR/DEST/ICSB 7      1    1 NRR/DEST/MEB     9H                   1    1      . NRR/DEST/MTB 9H      1    1 NRR/DEST/PSB     8D                   1    1        NRR/DEST/RSB 8E      1    1 NRR/DEST/SGB NRR/DLPQ/PEB
          .NRR D E     RPB 10 8D 10 1
1 2
1 1
2 NRR/DLPQ/HFB 10 NRR/DOEA/EAB 11 NUDOCS-ABSTRACT 1,1 1
1 1
1 1     1       RES/DSIR/EIB          1     1 RGN2      FILE    01                    1     1 EXTERNAL: EG&G WILLIAMS,S                          4    4        L ST LOBBY  WARD      1     1 LPDR                                    1     1       NRC PDR              1     1 NSIC MAYS,G                            1     1       NSIC MURPHY,G.A      1     1 NUDOCS FULL TXT                        1     1 NOXF TO ALL '%ZC6" RECIPIENTS'IZASE HELP US 'IO REXQCB             %@PTER   QMIRCT THE DOCUMENI'GNTBOL DESK RXH Pl-37 (EXT. 20079) m                   ELIMINAXB YOUR NAME PKH DISTEGBVX'ION.
LISTS HXR DOCUMENTS YOU DCK'T NEEDf FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR                             39 ENCL     39


====3.0.1 which====
P.O. Box14000, Juno Beach, FL 33408-0420 SEPTEMBER    2 2 1989 L-89-347 10 CFR 50.73 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C.                20555 Gentlemen:
states, in part,"When a Limiting Condition for Operation is not met, except as provided in the associated ACTION requirements, within 1 hour action shall be initiated to place the unit in a MODE in which the specifica-tion does not apply...".
Re:    Turkey Point Unit 4 Docket No. 50-251 Reportable Event: 89-09 Date of Event: August 23, 1989 Boric Acid Transfer Pump Seal Pot Found With No Visible Level Resulting in No Flow Path From the Boric Acid Tank to Unit 4 Reactor Coolant S stem The  attached Licensee Event Report is being submitted pursuant to the requirements of 10 CFR 50.73 to provide notification of the subject event.
Following the discovery, the 4B BATP seal pot was re-filled and pump flow was verified.The seal pot level was observed to remain stable.This was accomplished 33 minutes later at 1748, and Unit 4 exited Technical Specification 3.0.1.Cause of the Event The cause of this event is most likely attributable to the design of the BATP double seals.FPL believes that frequent pump starts and stops may cause axial shaft movement which results in separation of the inner seal faces.When the 4B BATP stopped automatic make-up to the Volume Control Tank at approximately 1700 on August 23, 1989, FPL believes the inner seal faces temporarily"cocked", resulting in a drain of seal water into the pump casing.Upon discovery of the low water level on the 4B BATP seal pot, operations per-sonnel inspected the BATP area.No evidence of seal water leakage from the seal pot drain valve, the 4B BATP outer seal, or from.any seal water system fittings was identified.
Very  truly      yours, J. H. Goldberg l Executive Vice President JHG/JRH/cm cc:    Stewart D. Ebneter, Regional Administrator, Region II,                USNRC Senior Resident Inspector, USNRC, Turkey Point Plant PDR  ADOC~
After adding water to the seal pot an verifying pump flow, the seal pot level was observed to remain stable.Anal sis of the Event Sufficient shutdown capability for the most severe anticipated cooldown trans-ient (main steam line break), assuming the most reactive control cluster is fully withdrawn, is achieved via the use of boron from the refueling water stor-age tank through the safety in)ection system.This flow path is a normal align-ment required by Technical Specification 3.6.c.4.NRC FORM 388A (983)  
14  gyoy2 0-0002Z1 PDt.
~0~0 l I NPC Fmm 300A (94ll C LICENSEE E ENT REPORT ILER)TEXT CONTI A ION US.NUCLEAR REGULATORY COMMISSION APPROVED OMS NO.3ISOM104 EXPIRES: 8/3(/88 FACILITY NAME ('II OOCKET NVMSER (3I LER NUMSER (0(PACE (3)Turkey Point Unit 4 TEXT///nuun<<wed/0/Pduiwf.uw 000/and/HRC Ann 30843/(IT(YEAR~iM$:(o s o o o2 51 89 SSOI/SHTIAL:y67 HUMddn 0 0 9-RCVISIOH HUM00<<00 03 OF 0 3 The BATs and the BATPs provide a souice of concentrated boric acid to be added to the reactor coolant system to offset reactivity changes caused by normal plant operating transients, changes in power levels, and to maintain shutdown conditions
                                                                    /i/    (
.An additional means of providing borated water is from the refuel-ing water storage tank through the charging pumps to the RCS.Although a flow path from the BAT to the Unit 4 Reactor Coolant System (RCS)was not available, the flow path from the refueling water storage tank to the RCS was available throughout the event.The BATPs are required for 10CFR50, Appendix R transients and'or post-LOCA chemistry control.These transients do not require immediate boration, therefore, substantial time is available to realign the Unit 3 BATPs to supply water from the C BAT to the Unit 4 charging pumps'ased on the above, the health and safety of the public were not affected.Corrective Actions 1)The 4B BATP seal pot drain valve was opened and it was confirmed that the seal pot contained water.Maintenance personnel then added approximately two quarts of water to the 4B BATP seal pot to restore the level.2)Pump flow from the 4B BATP was verified and the seal pot level was observed to remain stable.A visual inspection of the 4B BATP following restoration of the seal pot level showed no signs of pump outer seal leakage.3)In LER 250/88-019, FPL made a commitment to evaluate the BATP seal design and initiate a modification to remove the seal pots.Due to the inability to locate an acceptable BATP seal which does not require seal cooling water, this commitment is hereby modified by FPL.FPL is continuing the review of alternate seal designs for the BATPs.As an interim measure to improve the present BATP seal water system design,'a plant change/modification (PC/M)will be issued by May 31, 1990.This PC/M will provide improved level indication for the seal pots and will pro-vide a means of adding make-up water without having to remove the seal pot nitrogen pressure indicator from service.Additional Information The BATPs are manufactured by Goulds, Inc., Model No.3196-ST-8.The, seals are manufactured by Durametallic.
an FPL Group company
Similar occurrences have been reported in LER 250/88-019, LER 250/88-005, and LER 250/87-017
 
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NRC Form 355                                                                                                                                            US. NUCLEAR AEOULATORY COMMISSION I(cd')                                                                                                                                                          AppRDYED DMR No. 31500101 EXPIRES: 5/31/55 LICENSEE EVENT REPORT ILERI DOCKET NVMSKA (2)                            PA FACILITY NAME (1)
Turkey Point Unit 4                                                                                              02 51            1  OF    p  3 TITLE Iel        I  1c              rans er            ump                                                    o    1 s1        e      eye                      ng 1n No      Flow Path From Boric Acid Tank                                    to Unit              4 Reactor Coolant System EVKNT DATE (5)                      LER NUMSEA (SI                            AEPOAT DATE (7)                                OTHER FACILITIES INVOLVED (SI MONTH      DAY      YEAR    YEAR    <cN SSOVSNTIAL tri5 NVMSKR
                                                                  /ted~
4C NVMSSR MONTH DAY                        YEAR              FACILITYNAMES                        DOCK ET NUM 5 5 R(SI 0    5  0    0    0 823          8 9      8 9            009                  0    00          9    22 89                                                                  0    5  0    0    0 THIS REPORT IS SUSMITTKD PURSUANT T0              THE REQUIREMENTS OF 10 CFR g: /Chert one or more            of the foll~no/ (11 OPKAATINQ MODE (SI
                          ]        20A02()r I                                  20.405(cl                                50.73(el l2) (Ic)                            73.710r)
POTTER                          20AOS( ~ l(1)(0                              SOW(c) Ill                              50.73(e I (2) Ix)                            73.71(c)
LEVEL                                                                                                                                                              OTHEA /Specify /n Aptrrect IIOI      1      P P          20AOS(e) II ) (5)                            50.35(cl 12)                            50.73(e)12) ITS)
Pe/owenPIn Teer HRCFonn 20.405(el Ill(QII                            50.73(e) 12) Ill                        50.73(el(2) (vill)(AI                        3654/
Qr~<%                      20405 le)(1) IN)                            50.73(cl(2)(5)                          50.73(c) l2)(HIIIISI 20405(el(1)(c)                              50.73(e)12)(llil                        50.73(el(2) (x)
LICKNSEE CONTACT FOR THIS LER (12)
NAME                                                                                                                                                              TELEPHONE NVMSEA Oennis          W. Herrin, Regulation and Compliance Engineer                                                                          305 24 6-6 731 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE OKSCAISED IN THIS REPORT (13)
CAUSE    SYSTEM      COMPONENT MANVPAC TUAER
                                                                              '~~v '          N CAUSE SYSTEM    COMPONENT MANUFAC.
TVRER EPORTABLE TO NPROS K~A..      4 B    C A SE      AL              200                N                .: c n
                                                                                                    'mN ac~%
                                                                                                                                                                                  ~A%4
                                                                                          )v jc SUPPLEMENTAL REPORT EXPECTED (Ie)                                                                                        MONTH      OAY    YEAR EXPECTED SV 5 MISS I  ON DATE V5)
YES  Ilfyet, complete EXPECTED SVSSIISSIOH DATE/                                        NO ASSTAAOT ILlmit ro IFOO tpccet. I A. epproelmerely II/teen ring/ecpece lyf>>wr/tron llnnl (15)
On    August 23, 1989, at 1715, Unit 4 entered Technical Specification 3.0.1 for 33 minutes when the 4B Boric Acid Transfer Pump (BATP) was declared out of service. At the time of the event, the 4A BATP was out of service to repair a flange leak. At 1715, while making normal rounds, operations personnel discovered that the seal pot, which .pro-,
vides seal cooling water to the 4B BATP, had no visible water level.
Following the discovery, the 4B BATP seal pot was refilled and pump flow was verified . The seal pot level was observed, to remain stable.
This was completed after 33 minutes, and Unit 4 exited Technical Speci-fication 3.0.1. The cause of this event is most likely attributable to the design of the BATP double seals. FPL believes that frequent pump        starts and stops may cause axial shaft movement which results in separation of the inner seal faces. When the 4B BATP stopped automatic make-up to the Volume Control Tank at approximately 1700, FPL believes the inner seal faces temporarily "cocked", resulting in a drain of seal water into the pump casing. FPL engineering is continuing to re-view alternate seal designs for the BATPs which will not require quench water to the seal.
NAC Form 355
(%531
 
NRC.For~ 388A                                                                                  U.S. NUCLEAR REQULATORY COMMISSION I9>]l LICENS      )4T REPORT (LER) TEXT CONTI                                APPROVEO OMS NO. 3) 50M)04 EXPIRES: 8/3)/88 FACILITY NAME I) l                                  OOCKET NUMBER Ill                LER NUMSER I8)                    PAGE (3)
Turkey Point Unit 4                                                        YEAR Q>g EEOUENTIAL NUM \R    sgrg ~EVISIOH
                                                                                                      '~:  NUMSC/I 0  5  0  0  0  2 5    8 9        009 0              0    02  oF 0  3 Deseri tion of the Event On    August 23, 1989, at 1715, Unit 4 entered Technical Specification 3.0.1 for 33 minutes when the 4B Boric Acid Transfer Pump (BATP) (EIIS:CA, Component:P) was declared out of service . Unit 4 was operating at 100 percent power with the -4A BATP out of service to repair a leak. At the time of this event, the 4B BATP was aligned to take suction from the C Boric Acid Tank (BAT) and dis-charge to the Unit 4 Charging Pumps, the 3A BATP was aligned to take suction from the A BAT and discharge to the Unit 3 Charging Pumps, and the 3B BATP was aligned to recirculate the        B BAT.
At 1715, the 4B BATP was declared out of service when Operations personnel making normal rounds discovered that the seal pot, which contains seal cool-ing water under Nitrogen (N2) pressure, had no visible water level . (These normal rounds are performed on a four hour interval.) Since the 4A BATP had previously been declared out of service, there was no flow path established from the BATs to the Unit 4 Reactor Coolant System (RCS). Technical Speci-fication 3.6.d requires that during power operation, "System piping, inter-locks and valves shall be operable to the extent of establishing one flow path from the boric acid tanks, and one flow path from the refueling water storage tank, to each Reactor Coolant System." Unit 4 entered Technical Specification 3.0.1 which states, in part, "When a Limiting Condition for Operation is not met, except as provided in the associated ACTION requirements, within 1 hour action shall be initiated to place the unit in a MODE in which the specifica-tion does not apply...". Following the discovery, the 4B BATP seal pot was re-filled and pump flow was verified. The seal pot level was observed to remain stable. This was accomplished 33 minutes later at 1748, and Unit 4 exited Technical Specification 3.0.1.
Cause     of the Event The cause     of this event is most likely attributable to the design of the BATP double seals.         FPL believes that frequent pump starts and stops may cause axial shaft movement which results in separation of the inner seal faces. When the 4B BATP stopped automatic make-up to the Volume Control Tank at approximately 1700 on August 23, 1989, FPL believes the inner seal faces temporarily "cocked",
resulting in a drain of seal water into the pump casing.
Upon     discovery of the low water level on the 4B BATP seal pot, operations per-sonnel inspected the BATP area. No evidence of seal water leakage from the seal pot drain valve, the 4B BATP outer seal, or from. any seal water system fittings was identified. After adding water to the seal pot an verifying pump flow, the seal pot level was observed to remain stable .
Anal     sis of the Event Sufficient     shutdown capability for the most severe anticipated cooldown trans-ient (main       steam line break), assuming the most reactive control cluster is fully withdrawn, is achieved via the use of boron from the refueling water stor-age tank through the safety in)ection system.                 This flow path is a normal align-ment required by       Technical Specification   3.6.c.4.
NRC FORM 388A (983)
 
    ~0 ~0 l
I
 
NPC Fmm 300A (94ll                                                                                                               US. NUCLEAR REGULATORY COMMISSION C                                   LICENSEE     E   ENT REPORT ILER) TEXT CONTI           A ION                   APPROVED OMS NO. 3ISOM104 EXPIRES: 8/3(/88 FACILITY NAME ('II                                                   OOCKET NVMSER (3I LER NUMSER (0(                   PACE (3)
YEAR ~iM$:( SSOI/SHTIAL:y67 RCVISIOH HUMddn      HUM00<<
Turkey Point Unit                   4 TEXT ///nuun <<wed /0 /Pduiwf. uw 000/and/HRC Ann 30843/ (IT(
o s   o   o o2 51 89                 0   0 900 03               OF     0 3 The BATs and             the BATPs provide a souice of concentrated boric acid to be added to the reactor coolant system to offset reactivity changes caused by normal plant operating transients, changes in power levels, and to maintain shutdown conditions . An additional means of providing borated water is from the refuel-ing water storage tank through the charging pumps to the RCS. Although a flow path from the BAT to the Unit 4 Reactor Coolant System (RCS) was not available, the flow path from the refueling water storage tank to the RCS was available throughout the event. The BATPs are required for 10CFR50, Appendix R transients and'or post-LOCA chemistry control. These transients do not require immediate boration, therefore, substantial time is available to realign the Unit 3 BATPs to supply water from the C BAT to the Unit 4 charging pumps'ased on the above, the health and safety of the public were not affected .
Corrective Actions
: 1)     The 4B BATP             seal pot drain valve was opened and               it was confirmed that the seal pot contained water. Maintenance personnel then added approximately two quarts of water to the 4B BATP seal pot to restore the level .
: 2)       Pump       flow from the 4B BATP was verified and the seal pot level was observed to remain stable . A visual inspection of the 4B BATP following restoration of the seal pot level showed no signs of pump outer seal leakage.
: 3)       In     LER     250/88-019, FPL             made a commitment       to evaluate the       BATP   seal design and     initiate         a modification to         remove the seal pots. Due to the inability to locate an acceptable BATP seal which does not require seal cooling water, this commitment is hereby modified by FPL. FPL is continuing the review of alternate seal designs for the BATPs.
As an       interim measure to improve the present BATP seal water system design,
                    'a   plant change/modification (PC/M) will be issued by May 31, 1990. This PC/M will provide improved level indication for the seal pots and will pro-vide a means of adding make-up water without having to remove the seal pot nitrogen pressure indicator from service .
Additional Information The BATPs are manufactured                         by Goulds, Inc ., Model No. 3196-ST-8 .               The,   seals are manufactured by Durametallic.
Similar occurrences                 have been reported         in   LER   250/88-019,   LER     250/88-005, and LER   250/87-017
                                        'AC FOAM 3dd4 (94(3 I}}

Latest revision as of 21:58, 3 February 2020

LER 89-009-00:on 890823,boric Acid Transfer Pump Seal Pot Found W/No Visible Level Resulting in No Flow Path to Rcs. Caused by Design of Boric Acid Transfer Pump Double Seals. Review Continuing for Alternate Seal design.W/890922 Ltr
ML17347B345
Person / Time
Site: Turkey Point NextEra Energy icon.png
Issue date: 09/22/1989
From: Goldberg J, Herrin D
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
L-89-347, LER-89-009-01, LER-89-9-1, NUDOCS 8909270114
Download: ML17347B345 (7)


Text

'CCE~mTED QBUTION DEMON+TION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS) e ACCESSION NBR:8909270114 DOC.DATE: 89/09/22 NOTARIZED: NO DOCKET FACIL:50-251 Turkey Point Plant, Unit 4, Florida Power and Light C 05000251 AUTH. NAME AUTHOR AFFILIATION HERRIN,D.W. Florida Power & Light Co.

GOLDBERG,J.H. Florida Power & Light Co.

RECIP.NAME RECIPIENT AFFILIATION k

SUBJECT:

LER 89-009-00:on 890823,boric acid transfer pump seal pot found w/no visible level resulting in no flow path..

W/8 ltr.

DISTRIBUTION CODE- IE22T COPIES RECEIVED:LTR TITLE: 50.73/50.9 Licensee Event Report (LER),

ENCL g SIZE:

Incident'Rpt, etc.

NOTES:

RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD2-2 LA 1 1 PD2-2 PD 1 1 EDISON,G 1 1 INTERNAL ACRS MICHELSON 1 1 ACRS MOELLER 2 2 ACRS WYLIE 1 1 AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DSP 2 2 DEDRO 1 1 NRR/DEST/CEB 8H 1 1 NRR/DEST/ESB 8D 1 1 NRR/DEST/ICSB 7 1 1 NRR/DEST/MEB 9H 1 1 . NRR/DEST/MTB 9H 1 1 NRR/DEST/PSB 8D 1 1 NRR/DEST/RSB 8E 1 1 NRR/DEST/SGB NRR/DLPQ/PEB

.NRR D E RPB 10 8D 10 1

1 2

1 1

2 NRR/DLPQ/HFB 10 NRR/DOEA/EAB 11 NUDOCS-ABSTRACT 1,1 1

1 1

1 1 1 RES/DSIR/EIB 1 1 RGN2 FILE 01 1 1 EXTERNAL: EG&G WILLIAMS,S 4 4 L ST LOBBY WARD 1 1 LPDR 1 1 NRC PDR 1 1 NSIC MAYS,G 1 1 NSIC MURPHY,G.A 1 1 NUDOCS FULL TXT 1 1 NOXF TO ALL '%ZC6" RECIPIENTS'IZASE HELP US 'IO REXQCB  %@PTER QMIRCT THE DOCUMENI'GNTBOL DESK RXH Pl-37 (EXT. 20079) m ELIMINAXB YOUR NAME PKH DISTEGBVX'ION.

LISTS HXR DOCUMENTS YOU DCK'T NEEDf FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 39 ENCL 39

P.O. Box14000, Juno Beach, FL 33408-0420 SEPTEMBER 2 2 1989 L-89-347 10 CFR 50.73 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555 Gentlemen:

Re: Turkey Point Unit 4 Docket No. 50-251 Reportable Event: 89-09 Date of Event: August 23, 1989 Boric Acid Transfer Pump Seal Pot Found With No Visible Level Resulting in No Flow Path From the Boric Acid Tank to Unit 4 Reactor Coolant S stem The attached Licensee Event Report is being submitted pursuant to the requirements of 10 CFR 50.73 to provide notification of the subject event.

Very truly yours, J. H. Goldberg l Executive Vice President JHG/JRH/cm cc: Stewart D. Ebneter, Regional Administrator, Region II, USNRC Senior Resident Inspector, USNRC, Turkey Point Plant PDR ADOC~

14 gyoy2 0-0002Z1 PDt.

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Turkey Point Unit 4 02 51 1 OF p 3 TITLE Iel I 1c rans er ump o 1 s1 e eye ng 1n No Flow Path From Boric Acid Tank to Unit 4 Reactor Coolant System EVKNT DATE (5) LER NUMSEA (SI AEPOAT DATE (7) OTHER FACILITIES INVOLVED (SI MONTH DAY YEAR YEAR <cN SSOVSNTIAL tri5 NVMSKR

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4C NVMSSR MONTH DAY YEAR FACILITYNAMES DOCK ET NUM 5 5 R(SI 0 5 0 0 0 823 8 9 8 9 009 0 00 9 22 89 0 5 0 0 0 THIS REPORT IS SUSMITTKD PURSUANT T0 THE REQUIREMENTS OF 10 CFR g: /Chert one or more of the foll~no/ (11 OPKAATINQ MODE (SI

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LICKNSEE CONTACT FOR THIS LER (12)

NAME TELEPHONE NVMSEA Oennis W. Herrin, Regulation and Compliance Engineer 305 24 6-6 731 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE OKSCAISED IN THIS REPORT (13)

CAUSE SYSTEM COMPONENT MANVPAC TUAER

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On August 23, 1989, at 1715, Unit 4 entered Technical Specification 3.0.1 for 33 minutes when the 4B Boric Acid Transfer Pump (BATP) was declared out of service. At the time of the event, the 4A BATP was out of service to repair a flange leak. At 1715, while making normal rounds, operations personnel discovered that the seal pot, which .pro-,

vides seal cooling water to the 4B BATP, had no visible water level.

Following the discovery, the 4B BATP seal pot was refilled and pump flow was verified . The seal pot level was observed, to remain stable.

This was completed after 33 minutes, and Unit 4 exited Technical Speci-fication 3.0.1. The cause of this event is most likely attributable to the design of the BATP double seals. FPL believes that frequent pump starts and stops may cause axial shaft movement which results in separation of the inner seal faces. When the 4B BATP stopped automatic make-up to the Volume Control Tank at approximately 1700, FPL believes the inner seal faces temporarily "cocked", resulting in a drain of seal water into the pump casing. FPL engineering is continuing to re-view alternate seal designs for the BATPs which will not require quench water to the seal.

NAC Form 355

(%531

NRC.For~ 388A U.S. NUCLEAR REQULATORY COMMISSION I9>]l LICENS )4T REPORT (LER) TEXT CONTI APPROVEO OMS NO. 3) 50M)04 EXPIRES: 8/3)/88 FACILITY NAME I) l OOCKET NUMBER Ill LER NUMSER I8) PAGE (3)

Turkey Point Unit 4 YEAR Q>g EEOUENTIAL NUM \R sgrg ~EVISIOH

'~: NUMSC/I 0 5 0 0 0 2 5 8 9 009 0 0 02 oF 0 3 Deseri tion of the Event On August 23, 1989, at 1715, Unit 4 entered Technical Specification 3.0.1 for 33 minutes when the 4B Boric Acid Transfer Pump (BATP) (EIIS:CA, Component:P) was declared out of service . Unit 4 was operating at 100 percent power with the -4A BATP out of service to repair a leak. At the time of this event, the 4B BATP was aligned to take suction from the C Boric Acid Tank (BAT) and dis-charge to the Unit 4 Charging Pumps, the 3A BATP was aligned to take suction from the A BAT and discharge to the Unit 3 Charging Pumps, and the 3B BATP was aligned to recirculate the B BAT.

At 1715, the 4B BATP was declared out of service when Operations personnel making normal rounds discovered that the seal pot, which contains seal cool-ing water under Nitrogen (N2) pressure, had no visible water level . (These normal rounds are performed on a four hour interval.) Since the 4A BATP had previously been declared out of service, there was no flow path established from the BATs to the Unit 4 Reactor Coolant System (RCS). Technical Speci-fication 3.6.d requires that during power operation, "System piping, inter-locks and valves shall be operable to the extent of establishing one flow path from the boric acid tanks, and one flow path from the refueling water storage tank, to each Reactor Coolant System." Unit 4 entered Technical Specification 3.0.1 which states, in part, "When a Limiting Condition for Operation is not met, except as provided in the associated ACTION requirements, within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> action shall be initiated to place the unit in a MODE in which the specifica-tion does not apply...". Following the discovery, the 4B BATP seal pot was re-filled and pump flow was verified. The seal pot level was observed to remain stable. This was accomplished 33 minutes later at 1748, and Unit 4 exited Technical Specification 3.0.1.

Cause of the Event The cause of this event is most likely attributable to the design of the BATP double seals. FPL believes that frequent pump starts and stops may cause axial shaft movement which results in separation of the inner seal faces. When the 4B BATP stopped automatic make-up to the Volume Control Tank at approximately 1700 on August 23, 1989, FPL believes the inner seal faces temporarily "cocked",

resulting in a drain of seal water into the pump casing.

Upon discovery of the low water level on the 4B BATP seal pot, operations per-sonnel inspected the BATP area. No evidence of seal water leakage from the seal pot drain valve, the 4B BATP outer seal, or from. any seal water system fittings was identified. After adding water to the seal pot an verifying pump flow, the seal pot level was observed to remain stable .

Anal sis of the Event Sufficient shutdown capability for the most severe anticipated cooldown trans-ient (main steam line break), assuming the most reactive control cluster is fully withdrawn, is achieved via the use of boron from the refueling water stor-age tank through the safety in)ection system. This flow path is a normal align-ment required by Technical Specification 3.6.c.4.

NRC FORM 388A (983)

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I

NPC Fmm 300A (94ll US. NUCLEAR REGULATORY COMMISSION C LICENSEE E ENT REPORT ILER) TEXT CONTI A ION APPROVED OMS NO. 3ISOM104 EXPIRES: 8/3(/88 FACILITY NAME ('II OOCKET NVMSER (3I LER NUMSER (0( PACE (3)

YEAR ~iM$:( SSOI/SHTIAL:y67 RCVISIOH HUMddn HUM00<<

Turkey Point Unit 4 TEXT ///nuun <<wed /0 /Pduiwf. uw 000/and/HRC Ann 30843/ (IT(

o s o o o2 51 89 0 0 900 03 OF 0 3 The BATs and the BATPs provide a souice of concentrated boric acid to be added to the reactor coolant system to offset reactivity changes caused by normal plant operating transients, changes in power levels, and to maintain shutdown conditions . An additional means of providing borated water is from the refuel-ing water storage tank through the charging pumps to the RCS. Although a flow path from the BAT to the Unit 4 Reactor Coolant System (RCS) was not available, the flow path from the refueling water storage tank to the RCS was available throughout the event. The BATPs are required for 10CFR50, Appendix R transients and'or post-LOCA chemistry control. These transients do not require immediate boration, therefore, substantial time is available to realign the Unit 3 BATPs to supply water from the C BAT to the Unit 4 charging pumps'ased on the above, the health and safety of the public were not affected .

Corrective Actions

1) The 4B BATP seal pot drain valve was opened and it was confirmed that the seal pot contained water. Maintenance personnel then added approximately two quarts of water to the 4B BATP seal pot to restore the level .
2) Pump flow from the 4B BATP was verified and the seal pot level was observed to remain stable . A visual inspection of the 4B BATP following restoration of the seal pot level showed no signs of pump outer seal leakage.
3) In LER 250/88-019, FPL made a commitment to evaluate the BATP seal design and initiate a modification to remove the seal pots. Due to the inability to locate an acceptable BATP seal which does not require seal cooling water, this commitment is hereby modified by FPL. FPL is continuing the review of alternate seal designs for the BATPs.

As an interim measure to improve the present BATP seal water system design,

'a plant change/modification (PC/M) will be issued by May 31, 1990. This PC/M will provide improved level indication for the seal pots and will pro-vide a means of adding make-up water without having to remove the seal pot nitrogen pressure indicator from service .

Additional Information The BATPs are manufactured by Goulds, Inc ., Model No. 3196-ST-8 . The, seals are manufactured by Durametallic.

Similar occurrences have been reported in LER 250/88-019, LER 250/88-005, and LER 250/87-017

'AC FOAM 3dd4 (94(3 I