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{{#Wiki_filter:August 12, 2009 | {{#Wiki_filter:UNITED STATES | ||
NUC LE AR RE G UL AT O RY C O M M I S S I O N | |||
Wolf Creek Nuclear Operating Corporation P.O. Box 411 | R E GI ON I V | ||
612 EAST LAMAR BLVD , SU I TE 400 | |||
associated with the | AR LI N GTON , TEXAS 76011-4125 | ||
240°F, without providing adequate cooling of the suction headers to ensure that steam voiding would not occur if the residual heat removal system was needed for emergency core cooling system injection or recirculation. | August 12, 2009 | ||
management discretion, a decision was made that, although the risk for this event was in the overlap region, a focused baseline inspection would be performed since the risk for this issue was likely overestimated. The enclosed report documents the inspection results, which were discussed at the exit meeting on July 9, 2009, with Mr. Sunseri, Vice President Operations and Plant Manager, and other members of your staff. | Rick A. Muench, President and | ||
program, the NRC is treating these findings as noncited violations, consistent with Section I.A.1 of the NRC Enforcement Policy. | Chief Executive Officer | ||
Wolf Creek Nuclear Operating Corporation | |||
P.O. Box 411 | |||
Burlington, KS 66839 | |||
Subject: WOLF CREEK GENERATING STATION - NRC FOCUSED BASELINE INSPECTION | |||
REPORT 05000482/2009006 | |||
Dear Mr. Muench: | |||
On July 1, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed a focused baseline | |||
inspection at your Wolf Creek Generating Station. This inspection examined activities | |||
associated with the stations identification of a potential issue involving the likelihood of steam | |||
voiding the suction headers of both trains of the residual heat removal system if system | |||
actuation were required for injection or recirculation during Mode 3 operations. The genesis of | |||
this issue involved the stations practice of using both trains of the residual heat removal system | |||
for shutdown cooling while in Mode 4, with reactor coolant system temperature greater than | |||
240°F, without providing adequate cooling of the suction headers to ensure that steam voiding | |||
would not occur if the residual heat removal system was needed for emergency core cooling | |||
system injection or recirculation. | |||
The NRCs initial evaluation of this issue using the criteria in NRC Management Directive 8.3, | |||
NRC Incident Investigation Program, determined that the estimated Incremental Conditional | |||
Core Damage Probability was in the overlap region between a special inspection and an | |||
augmented inspection. However, it was determined that the model utilized likely over estimated | |||
the risk since this model was based on full power operations. Therefore, based on | |||
management discretion, a decision was made that, although the risk for this event was in the | |||
overlap region, a focused baseline inspection would be performed since the risk for this issue | |||
was likely overestimated. | |||
The enclosed report documents the inspection results, which were discussed at the exit meeting | |||
on July 9, 2009, with Mr. Sunseri, Vice President Operations and Plant Manager, and other | |||
members of your staff. The inspection examined activities conducted under your license as | |||
they relate to safety and compliance with the Commissions rules and regulations and with the | |||
conditions of your license. The inspection team reviewed selected procedures and records, | |||
observed activities, and interviewed personnel. | |||
This report documents two NRC identified findings of very low safety significance (Green). Both | |||
these findings were determined to involve violations of NRC requirements. However, because | |||
of their very low safety significance and because they were entered into your corrective action | |||
program, the NRC is treating these findings as noncited violations, consistent with Section I.A.1 | |||
of the NRC Enforcement Policy. If you contest the noncited violations in this report, you should | |||
Wolf Creek Nuclear Operating Corp. -2- | |||
provide a response within 30 days of the date of this inspection report, with the basis for your | |||
denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, | |||
Washington, D.C. 20555-0001, with copies to the Regional Administrator, U.S. Nuclear | |||
Wolf Creek | Regulatory Commission, Region IV, 612 E. Lamar Blvd, Suite 400, Arlington, Texas, | ||
76011-4125; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, | |||
Washington, D.C. 20555-0001; and the NRC Resident Inspector at the Wolf Creek Generating | |||
Station. In addition, if you disagree with the characterization of any finding in this report, you | |||
Wolf Creek | should provide a response within 30 days of the date of this inspection report, with the basis for | ||
your disagreement, to the Regional Administrator, Region IV, and the NRC Resident Inspector | |||
at Wolf Creek Generating Station. The information you provide will be considered in | |||
accordance with Inspection Manual Chapter 0305. | |||
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, and its | |||
enclosure, will be available electronically for public inspection in the NRC Public Document | |||
Room or from the Publicly Available Records component of NRCs document system (ADAMS). | |||
ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the | |||
Public Electronic Reading Room). | |||
Sincerely, | |||
/RA/ | |||
Vincent G. Gaddy, | |||
Chief, Project Branch B | |||
Division of Reactor Projects | |||
Docket: 50-482 | |||
Licenses: NPF-42 | |||
Enclosure: | |||
Enclosure: NRC Inspection Report 05000482/2009006 | |||
w/Attachment: Supplemental Information | |||
cc w/Enclosure: | |||
Vice President Operations/Plant Manager Chief Engineer | |||
Wolf Creek Nuclear Operating Corporation Utilities Division | |||
P.O. Box 411 Kansas Corporation Commission | |||
Burlington, KS 66839 1500 SW Arrowhead Road | |||
Topeka, KS 66604-4027 | |||
Jay Silberg, Esq. | |||
Pillsbury Winthrop Shaw Pittman LLP Office of the Governor | |||
2300 N Street, NW State of Kansas | |||
Washington, DC 20037 Topeka, KS 66612-1590 | |||
Supervisor Licensing Attorney General | |||
Wolf Creek Nuclear Operating Corporation 120 S.W. 10th Avenue, 2nd Floor | |||
P.O. Box 411 Topeka, KS 66612-1597 | |||
Burlington, KS 66839 | |||
Wolf Creek Nuclear Operating Corp. -3- | |||
County Clerk Chief, Technological Hazards | |||
Coffey County Courthouse Branch | |||
110 South 6th Street FEMA, Region VII | |||
Burlington, KS 66839 9221 Ward Parkway | |||
Suite 300 | |||
Chief, Radiation and Asbestos Kansas City, MO 64114-3372 | |||
Control Section | |||
Bureau of Air and Radiation | |||
Kansas Department of Health and | |||
Environment | |||
1000 SW Jackson, Suite 310 | |||
Topeka, KS 66612-1366 | |||
Wolf Creek Nuclear Operating Corp. -4- | |||
Electronic distribution by RIV: | |||
Regional Administrator (Elmo.Collins@nrc.gov) | |||
File located: | Deputy Regional Administrator (Chuck.Casto@nrc.gov) | ||
DRP Director (Dwight.Chamberlain@nrc.gov) | |||
DRP Deputy Director (Anton.Vegel@nrc.gov) | |||
DRS Director (Roy.Caniano@nrc.gov) | |||
DRS Deputy Director (Troy.Pruett@nrc.gov) | |||
Senior Resident Inspector (Chris.Long@nrc.gov) | |||
Resident Inspector (Charles.Peabody@nrc.gov) | |||
Site Secretary (Shirley.Allen@nrc.gov) | |||
Branch Chief, DRP/B (Vincent.Gaddy@nrc.gov) | |||
Senior Project Engineer, DRP/B (Rick.Deese@nrc.gov) | |||
Public Affairs Officer (Victor.Dricks@nrc.gov) | |||
Team Leader, DRP/TSS (Chuck.Paulk@nrc.gov) | |||
RITS Coordinator (Marisa.Herrera@nrc.gov) | |||
Regional Counsel (Karla.Fuller@nrc.gov) | |||
Congressional Affairs Officer (Jenny.Weil@nrc.gov) | |||
OEMail Resource | |||
Only inspection reports to the following: | |||
DRS STA (Dale.Powers@nrc.gov) | |||
OEDO RIV Coordinator (Leigh.Trocine@nrc.gov) | |||
ROPreports | |||
File located: R:\_REACTORS\_WC\2009\WC 2008-06 RP-JEJ Adams.doc ML 092240087 | |||
SUNSI Rev Compl. ;Yes No ADAMS ;Yes No Reviewer Initials | |||
Publicly Avail ;Yes No Sensitive Yes ;No Sens. Type Initials | |||
RI:DRP/E RI:DRS/EB1 SPE:DRP/B SRA:DRS/E | |||
JEJosey MRYoung RWDeese MRunyan | |||
VGG for /RA/ /RA/ /RA/ | |||
08/12/09 07/20/09 07/24/09 07/20/09 | |||
C:DRP/B | |||
VGGaddy | |||
/RA/ | |||
08/12/09 | |||
OFFICIAL RECORD COPY T= Telephone E= E-mail F = Fax | |||
U.S. NUCLEAR REGULATORY COMMISSION | |||
REGION IV | |||
Docket: 50-482 | |||
License: NPF-42 | |||
Report: 05000482/2009006 | |||
Licensee: Wolf Creek Operating Corporation | |||
Facility: Wolf Creek Generating Station | |||
Location: 1550 Oxen Lane SE | |||
Burlington, Kansas | |||
Dates: February 23 through July 1, 2009 | |||
Inspectors: J. Josey, Resident Inspector, Arkansas Nuclear One, Projects Branch E | |||
M. Runyan, Senior Reactor Analyst | |||
M. Young, Reactor Inspector | |||
A. Zoulis, Reliability and Risk Analyst, NRR/DRA/APOB | |||
Approved By: V. G. Gaddy, Chief, Project Branch B, Division of Reactor Projects | |||
-1- Enclosure | |||
SUMMARY OF FINDINGS | |||
IR 05000482/2009006; 02/23/09 - 07/01/09; Wolf Creek Generating Station, Focused Baseline | |||
Inspection in response to the identification of the potential to void the suction headers of both | |||
trains of the residual heat removal system on August 1, 2008. | |||
This report covered a 5-day period (February 23-27, 2009) of onsite inspection, with in office | |||
review through July 1, 2009. The focused baseline inspection team consisted of one resident | |||
inspector, one reactor inspector, and one senior reactor analyst. One Green noncited violation | |||
of significance was identified as well as one Green noncited Severity Level IV violation. The | |||
significance of most findings is indicated by their color (Green, White, Yellow, or Red) using | |||
NRC Inspection Manual Chapter 0609, "Significance Determination Process." Findings for | |||
which the significance determination process does not apply may be Green or be assigned a | |||
severity level after NRC management review. The NRC's program for overseeing the safe | |||
operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor | |||
Oversight Process," Revision 4, dated December 2006. | |||
A. NRC-Identified Findings and Self-Revealing Findings | |||
Cornerstone: Mitigating Systems | |||
* Green. The inspectors identified a noncited violation of Technical | |||
Specification 5.4.1, Procedures, associated with the licensees failure to ensure | |||
that adequate procedures were available for changing modes of operation of the | |||
residual heat removal system from shutdown cooling to emergency core cooling | |||
system operation. Specifically, station procedures allowed the residual heat | |||
removal system to be realigned to the emergency core cooling system mode of | |||
operation following operation in the shutdown cooling mode with suction | |||
temperatures as high as 350°F without properly cooling the entire suction header. | |||
This resulted in both trains of the residual heat removal system being inoperable | |||
during periods of operation in Modes 3 and 4. This issue was entered into the | |||
licensees corrective action program as Condition Reports 2008-3810 | |||
and 2008-4997. | |||
The performance deficiency was more than minor because it was associated with | |||
the equipment performance attribute of the Mitigating Systems Cornerstone and | |||
it directly affected the cornerstone objective to ensure the availability, reliability, | |||
and capability of systems that respond to initiating events to prevent undesirable | |||
consequences. Using Inspection Manual Chapter 0609, Significance | |||
Determination Process, Phase 1 Worksheet, the inspectors concluded that a | |||
Phase 2 evaluation was required because this finding represented a loss of | |||
safety function of the residual heat removal system. | |||
-2- Enclosure | |||
The inspectors performed a Phase 2 analysis using Appendix A, Determining | |||
the Safety Significance of Reactor Inspection Findings for At-Power Situations, | |||
of Inspection Manual Chapter 0609, Significance Determination Process, and | |||
the plant specific Phase 2 presolved tables and worksheets for Wolf Creek. The | |||
inspectors determined that the Phase 2 presolved tables and worksheets did not | |||
contain appropriate target sets to accurately estimate the risk input of the finding. | |||
Therefore, it was determined that a Phase 3 analysis was required. | |||
Senior risk analysts performed a Phase 3 analysis of this issue. The estimated | |||
Conditional Core Damage Probability was determined to be 2.84E-7, and the | |||
estimated Conditional Large Early Release Probability was determined to be | |||
2.72E-9. Based on these results, the finding was determined to be of very low | |||
safety significance. | |||
This finding was determined to have a crosscutting aspect in the area of Problem | |||
Identification and Resolution associated with the corrective action program | |||
[P.1(c)], in that the licensee failed to appropriately and thoroughly evaluate | |||
problems such that the resolutions address the causes (Section 2.2). | |||
Cornerstone: Miscellaneous | |||
* Severity Level IV. The inspectors identified a Severity Level IV noncited violation | |||
of 10 CFR 50.73, Licensee Event Report System, associated with the | |||
licensees failure to submit a licensee event report within 60 days following | |||
discovery of an event meeting the reportability criteria as specified. Specifically, | |||
on December 8, 2008, the licensee completed analysis of an issue associated | |||
with the residual heat removal system which determined that both trains of the | |||
system were inoperable when suction side temperature exceeded 249°F. Based | |||
on the results of this analysis as well as plant operating history, it was | |||
determined that the licensee failed to report instances where the system was | |||
operated in a condition prohibited by technical specifications, and a loss of safety | |||
function of the system existed between March 20, 2008, and December 8, 2008. | |||
Opened and Closed | Opened and Closed | ||
05000482/2009006-01 NCV Failure to Report Conditions Prohibited by Technical Specifications and Safety System Functional Failures 05000482/2009006-02 NCV Inadequate Instructions for Changing Modes of Operation of the Residual Heat Removal System | 05000482/2009006-01 NCV Failure to Report Conditions Prohibited by Technical | ||
Closed None | Specifications and Safety System Functional Failures | ||
05000482/2009006-02 NCV Inadequate Instructions for Changing Modes of Operation | |||
of the Residual Heat Removal System | |||
Closed | |||
None | |||
A-1 Attachment | |||
LIST OF DOCUMENTS REVIEWED | |||
PROCEDURES | PROCEDURES | ||
NUMBER TITLE REVISION | |||
SYS BG-216 Reactor Make-up Control System Alternate 24 | |||
Operation | |||
EMG C-11 Loss of Emergency Coolant Recirculation 20 | |||
EDMG-T01 EDMG Tool Box 4 | |||
EMG C-13 Control Room Response to Sump Blockage 2 | |||
OFN EJ-015 Loss of RHR Cooling 15A | |||
SYS EJ-121 Startup of a RHR Train in Cooldown Mode 21 | |||
SYS EJ-120 Startup of a Residual Heat Removal Train 51 | |||
GEN 00-006 Hot Standby to Cold Shutdown 68 | |||
GEN 00-008 Reduced Inventory Operations 18A | |||
AP 20E-001 Industry Operating Experience Program 12 | |||
AP 28A-100 Condition Reports 7 | |||
OFN EJ-40 CL Recirc During Mode 3, With Accumulators 2 | |||
Isolated, Mode 4, 5 or 6 | |||
EMG ES-11 Post LOCA Cooldown and Depressurization 14 | |||
EMG ES-12 Transfer to Cold Leg Recirculation 12 | |||
GEN 00-002 Cold Shutdown to Hot Standby 67A | |||
SYS EJ-320 Placing RHR System In Safety Injection Standby 32 | |||
Condition | |||
EP-01-2.1-1 Emergency Action Levels 10 | |||
EPP 01-2.1 Emergency Classification 18 | |||
OFN BB-031 Shutdown LOCA 9 | |||
STS EJ-100A RHR System Inservice Pump A Test 23 | |||
STS EJ-100B RHR System Inservice Pump B Test 19 | |||
SYS EJ-321 Shutdown of a Residual Heat Removal Train 23 | |||
SYS EJ-323 RHR System Depressurization 9 | |||
OFN NB-34 Loss of All AC Power - Shutdown Conditions 5 | |||
ALAR 00-050C RHR Loop 2 Flow Lo 10 | |||
ALAR 00-49C RHR Loop 2 Flow Lo 11 | |||
A-2 Attachment | |||
2008-5917 2009-0939 2009-1261 | CALCULATIONS | ||
NUMBER TITLE REVISION | |||
AN-01-025 No Title 0 | |||
AN-97-027 Time To Boil In The Core and Core Uncovery In 0 | |||
The Event of a Loss of RHR Cooling During | |||
Refueling 9 | |||
CONDITION REPORTS | |||
2007-2162 2008-2187 2008-2262 2008-4997 2008-5917 | |||
2007-2656 2008-0717 2008-3745 2008-5912 2009-0939 | |||
2008-0164 2008-0989 2008-3810 2008-5913 2009-1261 | |||
2008-0717 2008-2187 2008-4997 2008-5915 | |||
2008-0989 | |||
PERFORMANCE IMPROVEMENT REQUEST | |||
PIR 99-0228 PIR 2004-2440 | |||
MISCELLANOUS | |||
NUMBER TITLE REVISION | |||
NSAL-93-004 RHRS Operation as Part of the ECCS During Plant 0 | |||
Startup | |||
LER 2008-008-00 Potential for Residual Heat Removal Trains to be 0 | |||
Inoperable during Mode Change | |||
LER 2008-008-00 Potential for Residual Heat Removal Trains to be 1 | |||
Inoperable during Mode Change | |||
ITIP 02324 Westinghouse Letter SAP-93-706 (4-29-93): RHR 0 | |||
Operation As Part Of The ECCS During Plant | |||
Startup (Residual Heat Removal) (NSAL-93-004) | |||
ITIP 05342 Westinghouse InfoGram IG-04-6: Reactor Trip February 25, | |||
Breaker Auto Shunt Trip Test Panel. 2009 | |||
ITIP 05288 SER 3-04 - Reactor Overpower Events Associated February 25, | |||
with Ultrasonic Feedwater Flow Measurement 2009 | |||
Systems | |||
SEL 2009-135 Self Assessment Plan Industry Operating | |||
Experience Program | |||
Assessment 92 Assessment/Audit Detail Report Industry Operating September 21, | |||
Experience Program 2007 | |||
A-3 Attachment | |||
NUMBER TITLE REVISION | |||
Quick Hit Detail Report IOE Re-Evaluation Project | |||
1369 | |||
LTR-LIS-09-361 Engineering Report Wolf Creek Generating Station June 5, 2009 | |||
Modes 3 and 4 Loss-of-Coolant Accident Analysis | |||
For Residual Heat Removal Operability Study | |||
SY1300600 Emergency Core Cooling System 18 | |||
SY1300500 Residual Heat Removal 15 | |||
SY1505900 Feedwater System 16 | |||
SY1505900 Feedwater System 16 | SY1303200 Containment System 15 | ||
SY1303200 Containment System 15 | SY1300600 Emergency Core Cooling System 18 | ||
SY1300600 Emergency Core Cooling System 18 | SY1300400 Chemical Volume and Control System 22 | ||
SY1300400 Chemical Volume and Control System 22 | A-4 Attachment | ||
}} | }} |
Latest revision as of 03:17, 14 November 2019
ML092240087 | |
Person / Time | |
---|---|
Site: | Wolf Creek |
Issue date: | 08/12/2009 |
From: | Vincent Gaddy NRC/RGN-IV/DRP/RPB-B |
To: | Muench R Wolf Creek |
References | |
IR-09-006 | |
Download: ML092240087 (34) | |
See also: IR 05000482/2009006
Text
UNITED STATES
NUC LE AR RE G UL AT O RY C O M M I S S I O N
R E GI ON I V
612 EAST LAMAR BLVD , SU I TE 400
AR LI N GTON , TEXAS 76011-4125
August 12, 2009
Rick A. Muench, President and
Chief Executive Officer
Wolf Creek Nuclear Operating Corporation
P.O. Box 411
Burlington, KS 66839
Subject: WOLF CREEK GENERATING STATION - NRC FOCUSED BASELINE INSPECTION
REPORT 05000482/2009006
Dear Mr. Muench:
On July 1, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed a focused baseline
inspection at your Wolf Creek Generating Station. This inspection examined activities
associated with the stations identification of a potential issue involving the likelihood of steam
voiding the suction headers of both trains of the residual heat removal system if system
actuation were required for injection or recirculation during Mode 3 operations. The genesis of
this issue involved the stations practice of using both trains of the residual heat removal system
for shutdown cooling while in Mode 4, with reactor coolant system temperature greater than
240°F, without providing adequate cooling of the suction headers to ensure that steam voiding
would not occur if the residual heat removal system was needed for emergency core cooling
system injection or recirculation.
The NRCs initial evaluation of this issue using the criteria in NRC Management Directive 8.3,
NRC Incident Investigation Program, determined that the estimated Incremental Conditional
Core Damage Probability was in the overlap region between a special inspection and an
augmented inspection. However, it was determined that the model utilized likely over estimated
the risk since this model was based on full power operations. Therefore, based on
management discretion, a decision was made that, although the risk for this event was in the
overlap region, a focused baseline inspection would be performed since the risk for this issue
was likely overestimated.
The enclosed report documents the inspection results, which were discussed at the exit meeting
on July 9, 2009, with Mr. Sunseri, Vice President Operations and Plant Manager, and other
members of your staff. The inspection examined activities conducted under your license as
they relate to safety and compliance with the Commissions rules and regulations and with the
conditions of your license. The inspection team reviewed selected procedures and records,
observed activities, and interviewed personnel.
This report documents two NRC identified findings of very low safety significance (Green). Both
these findings were determined to involve violations of NRC requirements. However, because
of their very low safety significance and because they were entered into your corrective action
program, the NRC is treating these findings as noncited violations, consistent with Section I.A.1
of the NRC Enforcement Policy. If you contest the noncited violations in this report, you should
Wolf Creek Nuclear Operating Corp. -2-
provide a response within 30 days of the date of this inspection report, with the basis for your
denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,
Washington, D.C. 20555-0001, with copies to the Regional Administrator, U.S. Nuclear
Regulatory Commission, Region IV, 612 E. Lamar Blvd, Suite 400, Arlington, Texas,
76011-4125; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission,
Washington, D.C. 20555-0001; and the NRC Resident Inspector at the Wolf Creek Generating
Station. In addition, if you disagree with the characterization of any finding in this report, you
should provide a response within 30 days of the date of this inspection report, with the basis for
your disagreement, to the Regional Administrator, Region IV, and the NRC Resident Inspector
at Wolf Creek Generating Station. The information you provide will be considered in
accordance with Inspection Manual Chapter 0305.
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, and its
enclosure, will be available electronically for public inspection in the NRC Public Document
Room or from the Publicly Available Records component of NRCs document system (ADAMS).
ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the
Public Electronic Reading Room).
Sincerely,
/RA/
Vincent G. Gaddy,
Chief, Project Branch B
Division of Reactor Projects
Docket: 50-482
Licenses: NPF-42
Enclosure:
Enclosure: NRC Inspection Report 05000482/2009006
w/Attachment: Supplemental Information
cc w/Enclosure:
Vice President Operations/Plant Manager Chief Engineer
Wolf Creek Nuclear Operating Corporation Utilities Division
P.O. Box 411 Kansas Corporation Commission
Burlington, KS 66839 1500 SW Arrowhead Road
Topeka, KS 66604-4027
Jay Silberg, Esq.
Pillsbury Winthrop Shaw Pittman LLP Office of the Governor
2300 N Street, NW State of Kansas
Washington, DC 20037 Topeka, KS 66612-1590
Supervisor Licensing Attorney General
Wolf Creek Nuclear Operating Corporation 120 S.W. 10th Avenue, 2nd Floor
P.O. Box 411 Topeka, KS 66612-1597
Burlington, KS 66839
Wolf Creek Nuclear Operating Corp. -3-
County Clerk Chief, Technological Hazards
Coffey County Courthouse Branch
110 South 6th Street FEMA, Region VII
Burlington, KS 66839 9221 Ward Parkway
Suite 300
Chief, Radiation and Asbestos Kansas City, MO 64114-3372
Control Section
Bureau of Air and Radiation
Kansas Department of Health and
Environment
1000 SW Jackson, Suite 310
Topeka, KS 66612-1366
Wolf Creek Nuclear Operating Corp. -4-
Electronic distribution by RIV:
Regional Administrator (Elmo.Collins@nrc.gov)
Deputy Regional Administrator (Chuck.Casto@nrc.gov)
DRP Director (Dwight.Chamberlain@nrc.gov)
DRP Deputy Director (Anton.Vegel@nrc.gov)
DRS Director (Roy.Caniano@nrc.gov)
DRS Deputy Director (Troy.Pruett@nrc.gov)
Senior Resident Inspector (Chris.Long@nrc.gov)
Resident Inspector (Charles.Peabody@nrc.gov)
Site Secretary (Shirley.Allen@nrc.gov)
Branch Chief, DRP/B (Vincent.Gaddy@nrc.gov)
Senior Project Engineer, DRP/B (Rick.Deese@nrc.gov)
Public Affairs Officer (Victor.Dricks@nrc.gov)
Team Leader, DRP/TSS (Chuck.Paulk@nrc.gov)
RITS Coordinator (Marisa.Herrera@nrc.gov)
Regional Counsel (Karla.Fuller@nrc.gov)
Congressional Affairs Officer (Jenny.Weil@nrc.gov)
OEMail Resource
Only inspection reports to the following:
OEDO RIV Coordinator (Leigh.Trocine@nrc.gov)
ROPreports
File located: R:\_REACTORS\_WC\2009\WC 2008-06 RP-JEJ Adams.doc ML 092240087
SUNSI Rev Compl. ;Yes No ADAMS ;Yes No Reviewer Initials
Publicly Avail ;Yes No Sensitive Yes ;No Sens. Type Initials
RI:DRP/E RI:DRS/EB1 SPE:DRP/B SRA:DRS/E
JEJosey MRYoung RWDeese MRunyan
VGG for /RA/ /RA/ /RA/
08/12/09 07/20/09 07/24/09 07/20/09
C:DRP/B
VGGaddy
/RA/
08/12/09
OFFICIAL RECORD COPY T= Telephone E= E-mail F = Fax
U.S. NUCLEAR REGULATORY COMMISSION
REGION IV
Docket: 50-482
License: NPF-42
Report: 05000482/2009006
Licensee: Wolf Creek Operating Corporation
Facility: Wolf Creek Generating Station
Location: 1550 Oxen Lane SE
Burlington, Kansas
Dates: February 23 through July 1, 2009
Inspectors: J. Josey, Resident Inspector, Arkansas Nuclear One, Projects Branch E
M. Runyan, Senior Reactor Analyst
M. Young, Reactor Inspector
A. Zoulis, Reliability and Risk Analyst, NRR/DRA/APOB
Approved By: V. G. Gaddy, Chief, Project Branch B, Division of Reactor Projects
-1- Enclosure
SUMMARY OF FINDINGS
IR 05000482/2009006; 02/23/09 - 07/01/09; Wolf Creek Generating Station, Focused Baseline
Inspection in response to the identification of the potential to void the suction headers of both
trains of the residual heat removal system on August 1, 2008.
This report covered a 5-day period (February 23-27, 2009) of onsite inspection, with in office
review through July 1, 2009. The focused baseline inspection team consisted of one resident
inspector, one reactor inspector, and one senior reactor analyst. One Green noncited violation
of significance was identified as well as one Green noncited Severity Level IV violation. The
significance of most findings is indicated by their color (Green, White, Yellow, or Red) using
NRC Inspection Manual Chapter 0609, "Significance Determination Process." Findings for
which the significance determination process does not apply may be Green or be assigned a
severity level after NRC management review. The NRC's program for overseeing the safe
operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor
Oversight Process," Revision 4, dated December 2006.
A. NRC-Identified Findings and Self-Revealing Findings
Cornerstone: Mitigating Systems
- Green. The inspectors identified a noncited violation of Technical
Specification 5.4.1, Procedures, associated with the licensees failure to ensure
that adequate procedures were available for changing modes of operation of the
residual heat removal system from shutdown cooling to emergency core cooling
system operation. Specifically, station procedures allowed the residual heat
removal system to be realigned to the emergency core cooling system mode of
operation following operation in the shutdown cooling mode with suction
temperatures as high as 350°F without properly cooling the entire suction header.
This resulted in both trains of the residual heat removal system being inoperable
during periods of operation in Modes 3 and 4. This issue was entered into the
licensees corrective action program as Condition Reports 2008-3810
and 2008-4997.
The performance deficiency was more than minor because it was associated with
the equipment performance attribute of the Mitigating Systems Cornerstone and
it directly affected the cornerstone objective to ensure the availability, reliability,
and capability of systems that respond to initiating events to prevent undesirable
consequences. Using Inspection Manual Chapter 0609, Significance
Determination Process, Phase 1 Worksheet, the inspectors concluded that a
Phase 2 evaluation was required because this finding represented a loss of
safety function of the residual heat removal system.
-2- Enclosure
The inspectors performed a Phase 2 analysis using Appendix A, Determining
the Safety Significance of Reactor Inspection Findings for At-Power Situations,
of Inspection Manual Chapter 0609, Significance Determination Process, and
the plant specific Phase 2 presolved tables and worksheets for Wolf Creek. The
inspectors determined that the Phase 2 presolved tables and worksheets did not
contain appropriate target sets to accurately estimate the risk input of the finding.
Therefore, it was determined that a Phase 3 analysis was required.
Senior risk analysts performed a Phase 3 analysis of this issue. The estimated
Conditional Core Damage Probability was determined to be 2.84E-7, and the
estimated Conditional Large Early Release Probability was determined to be
2.72E-9. Based on these results, the finding was determined to be of very low
safety significance.
This finding was determined to have a crosscutting aspect in the area of Problem
Identification and Resolution associated with the corrective action program
P.1(c), in that the licensee failed to appropriately and thoroughly evaluate
problems such that the resolutions address the causes (Section 2.2).
Cornerstone: Miscellaneous
- Severity Level IV. The inspectors identified a Severity Level IV noncited violation
of 10 CFR 50.73, Licensee Event Report System, associated with the
licensees failure to submit a licensee event report within 60 days following
discovery of an event meeting the reportability criteria as specified. Specifically,
on December 8, 2008, the licensee completed analysis of an issue associated
with the residual heat removal system which determined that both trains of the
system were inoperable when suction side temperature exceeded 249°F. Based
on the results of this analysis as well as plant operating history, it was
determined that the licensee failed to report instances where the system was
operated in a condition prohibited by technical specifications, and a loss of safety
function of the system existed between March 20, 2008, and December 8, 2008.
The licensee entered this issue into their corrective action program as Condition
Reports 2009-1261 and 2009-1326 and Action Requests 15244, 17776,
and 15306.
The inspectors reviewed this issue in accordance with Inspection Manual
Chapter 0612 and the NRC Enforcement Manual. Through this review, the
inspectors determined that traditional enforcement was applicable to this issue
because the NRC's regulatory ability was affected. Specifically, the NRC relies
on licensee to identify and report conditions or events meeting the criteria
specified in regulations in order to perform its regulatory function, and when this
is not done, the regulatory function is impacted. The inspectors determined that
this finding was not suitable for evaluation using the significance determination
process, and as such, was evaluated in accordance with the NRC Enforcement
Policy. The finding was reviewed by NRC management and, because the
violation was determined to be of very low safety significance, was not repetitive
or willful, and was entered into the corrective action program, this violation is
being treated as a Severity Level IV noncited violation consistent with the NRC
Enforcement Policy. This finding was determined to have a crosscutting aspect
in the area of Problem Identification and Resolution associated with the
-3- Enclosure
corrective action program in that the licensee failed to appropriately and
thoroughly evaluate for reportability aspects all factors and time frames
associated with the inoperability of residual heat removal system when suction
temperatures were above 249°F P.1(c)(Section 2.1).
B. Licensee-Identified Violations
None.
-4- Enclosure
Report Details
1.0 Focused Baseline Inspection Scope
The NRC conducted a focused baseline inspection at the Wolf Creek Generating Station
to better understand the identification of a potential issue involving the likelihood of
steam voiding the suction headers of both trains of the residual heat removal system if
system actuation were required for injection or recirculation during Mode 3 operations.
The genesis of this issue involved the stations practice of using both trains of the
residual heat removal system for shutdown cooling while in Mode 4, with reactor coolant
system temperature greater than 240°F, without providing adequate cooling of the
suction headers to ensure that steam voiding would not occur if the residual heat
removal system was needed for emergency core cooling system injection or
recirculation.
On August 1, 2008, station personnel generated Condition Report 2008-810 to identify
this issue and evaluate potential system impacts due to the potential inoperability of the
residual heat removal system. Subsequently, the stations evaluation determined that
the historical operating practices for the residual heat removal system had resulted in
past inoperability of both trains of the system. This resulted in the licensee issuing
Licensee Event Report 5000482/2008008-00 in October 2008.
NRC managements initial evaluation of this issue, using the criteria in NRC
Management Directive 8.3, NRC Incident Investigation Program, determined that the
estimated incremental conditional core damage probability was in the overlap region
between a special inspection and an augmented inspection. However, it was
determined that the model utilized to analyze this issue likely overestimated the risk
since this model was based on station full power operations. Therefore, based on
management discretion, a decision was made that, although the risk for this event was in
the overlap region due to the likelihood of overestimation, a focused baseline inspection
would be performed to determine the full extent of this issue including determination of
risk.
For this inspection, the Focused Baseline Inspection team used NRC Inspection
Procedure 7111115, Operability Evaluations; Procedure 71152, Identification and
Resolution of Problems; and Procedure 71153, Followup of Events and Notices of
Enforcement Discretion. The team reviewed station procedures, corrective action
documents, engineering evaluations and design documentation for the residual heat
removal system as well as interviewing various station personnel regarding this issue.
The team also reviewed the licensees root cause analysis, extent of condition
evaluation, immediate and long term corrective actions, and industry operating
experience. A list of the specific documents reviewed is provided in Attachment 1.
Background
Gas accumulation or voiding of safety-related fluid systems can cause air binding in
pumps or water hammer events in piping systems. Instances of gas accumulation or
voiding in safety-related fluid systems have occurred on several instances in the nuclear
industry, and as a result, the NRC has published 20 information notices, 2 generic
letters, and a NUREG related to this issue, as well as interacting with the nuclear
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industry in relation to these publications and in response to gas accumulation/voiding
events.
It is important that systems relied upon to mitigate accidents and events are able to
perform their designed safety function. Specifically, a fluid system whose successful
operation is dependant upon the proper operation of a pump to be able to inject water
should be sufficiently filled to ensure that it can reliably perform its intended function
under all accident and nonaccident conditions as required.
Inadequate control of gas introduction or void formation in a fluid system can have the
following safety implications:
- The introduction of gases into a pump can cause the pump to become air bound
which results in little to no flow being generated by the pump, rendering the
pump inoperable. An air bound pump can become damaged quickly, thereby
eliminating the possibility of recovering the pump during an event by venting the
pump casing and suction piping.
- Gas introduction into a pump can render a pump inoperable, even if the gas does
not air bind the pump. This occurs when there is gas accumulation in the pump
casing which reduces the pump's discharge pressure and flow capacity to the
point that the pump can no longer perform its design safety function.
- Void formation and gas accumulation can also result in a system pressure
transient event known as water hammer. This is most commonly seen in the
discharge piping, but can also occur in the suction piping. This phenomenon
occurs when a pressure surge or wave is generated when a fluid in motion is
forced to suddenly stop or change direction. Specifically, when there is a rapid
venting or void collapse in a system, followed by a rapid refill of the piping with
water, there is the potential to have water hammer due to the system
configuration.
- Time needed to vent and refill voided discharge piping could delay delivery of
water from the system beyond the timeframe assumed in the facilities safety
analysis.
1.1 Event Summary
On January 18, 2008, the licensee initiated Condition Report 2008-0164 to address
NRC Generic Letter 2008-001, Managing Gas Accumulation in Emergency Core
Cooling, Decay Heat Removal, and Containment Spray Systems.
On March 21, 2008, station personnel generated Condition Report 2008-0989 based on
questions raised by an individual from the Callaway Plant, the sister unit to Wolf Creek
who was performing a benchmarking trip at the Wolf Creek Station. After observing the
reactor coolant system cooldown in preparation for a refueling outage, the individual
observed that station procedures allowed for both residual heat removal trains to be
aligned in shutdown cooling mode with reactor coolant system temperature above 260°F,
which was different than what was allowed by Callaway station procedures. Specifically,
the individual noted that in Callaways last operating cycle station procedures were
changed so that only one residual heat removal train could be aligned for shutdown
cooling with reactor coolant system temperature above 260°F, and the other train must
-6- Enclosure
remain aligned to the refueling water storage tank, which was the emergency core
cooling system injection lineup. The basis for this change was due to a concern of
potential flashing in the residual heat removal systems suction piping if the pressure of
the system was reduced following realignment to the refueling water storage tank.
The licensees evaluation of this issue concluded that the current practices associated
with the residual heat removal system were acceptable and allowed by technical
specifications. This was based on the licensees review and interpretation of the
facilities technical specifications requirements for residual heat removal system
alignment, verification that station procedures required cooldown of the residual heat
removal suction prior to alignment to the refueling water storage tank, and information
contained in Westinghouse Document WCAP-12476, Evaluation of LOCA During
Mode 3 and 4 Operation for Westinghouse NSSS.
On May 10, 2008, following maintenance to correct flange leaks on the residual heat
removal Pump B discharge flange and refueling water storage tank check valve, the
system was aligned to the reactor coolant system, as part of the retest, to place reactor
coolant system pressure on the affected joints. Subsequently, the pump was secured
and the train was realigned to take suction from the refueling water storage tank. At this
point the licensee attempted to perform ultrasonic testing of the residual heat removal
piping to check for voids, but found that the piping was too hot to attach the required
instrumentation. The licensee decided to vent the piping in an effort to reduce
temperature and vented a mixture of steam and water for approximately 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> before
the suction piping became water solid. The licensee initiated Station Work
Order 08-306203-000 to perform troubleshooting to determine if the suction piping
temperature was below saturation temperature where the recirculation line taps into the
system. (This issue was not entered into the licensees corrective action program.)
During the stations evaluation of Condition Report 2008-0164, an operations
representative identified a concern with the potential for steam binding. Specifically,
steam voiding concerns that had been identified during restoration of the residual heat
removal system at the end of Refueling Outage 16, on May 10, 2008, which could
happen any time the station enters Mode 3, combined with the findings from the generic
letter review prompted the initiation of another condition report to review these concerns.
On August 1, 2008, station personnel initiated Condition Report 2008-3810 to address
concerns that had been identified during the review for Generic Letter 2008-01 regarding
potential void formation. This condition report questioned the past operability of the
residual heat removal system when aligned in the injection mode with suction piping
temperature as high as 350°F, as well as the current design adequacy to ensure cooling
of suction piping using the mini-flow recirculation line. An evaluation was requested to
determine the effects of potential steam voiding in the residual heat removal suction
piping when realigning the system from reactor coolant system cooling to emergency
core cooling system injection while transitioning from Mode 4 to Mode 3.
On September 23, 2008, Wolf Creek completed their evaluation of the potential voiding
issue identified in Condition Report 2008-3810. The conclusions that were reached
were recirculation cannot be relied upon to cool the water in the isolated suction line, the
residual heat removal system would not have functioned if a loss of coolant accident had
occurred in Mode 3 with elevated suction piping fluid temperature, and the residual heat
removal train used for shutdown cooling should be secured, or put in service, only at a
-7- Enclosure
temperature of 240°F to ensure operability. Based on these conclusions, on October 3,
2008, Wolf Creek submitted Licensee Event Report 05000482/2008008-00 in
accordance with 10 CFR 50.73.
On October 10, 2008, the licensee initiated Condition Report 2008-4997, Missed
Opportunity to Resolve RHR Suction Piping Issue, for the purpose of determining why
two separate conditions initiated for apparently the same issue came to different
conclusions. This condition report was also used to perform a root cause analysis of the
potential voiding issue associated with the residual heat removal system as well as
performing a past operability review.
On December 5, 2008, Wolf Creek completed their evaluations as directed by Condition
Report 2008-4997. The evaluations concluded:
- From a past operability perspective, the residual heat removal system must be
considered inoperable any time the plant was in Mode 4 with the reactor coolant
system suction isolation valves open and reactor coolant system temperature
was above 249.1°F.
- The residual heat removal system must be considered inoperable in Mode 3
during plant heatup for a period of 46 hours5.324074e-4 days <br />0.0128 hours <br />7.60582e-5 weeks <br />1.7503e-5 months <br /> following isolation from the reactor
coolant system. This is based on the amount of time it would take the suction
piping and fluid to cool down to 225°F.
- From the perspective of past functionality, the residual heat removal system
would not have been functional during a small break loss of coolant accident in
Modes 3 or 4, nor a large break loss of coolant accident in Mode 3 for injection or
recirculation.
Based on these conclusions, on January 30, 2009, Wolf Creek submitted an updated
Licensee Event Report 05000482/2008008-01.
The team constructed the following time line of events relative to the issue:
Date Details
March 1990 Wolf Creek received Westinghouse Report WOG-90-048,
Residual heat removal System Operability During a Mode 4
LOCA. The purpose of this report was to detail the efforts taken
by Westinghouse to evaluate residual heat removal system
operability and potential water hammer concerns following a loss
of coolant accident during Mode 4 operations. The report stated
that the concern of hot residual heat removal pump suction fluid
being trapped by the refueling water storage tank to residual
heat removal system check valve, and the condition of rapid
depressurization of saturated water during a pump start producing
a large void fraction in the suction piping. This was an
informational report that required no response and no action on
behalf of the licensee.
-8- Enclosure
June 1990 Wolf Creek received Letter OG-90-30, Shutdown LOCA
Concerns that Relate to the Interim Guidance. The purpose of
this letter was to inform all Westinghouse Owner Group utilities of
the new shutdown loss of coolant accident concerns identified
since the interim guidance was issued in 1987. This letter formally
identified the two new concerns previously identified in the
Westinghouse Report WOG-0-48, Residual Heat Removal
System Operability During a Mode Loss of Coolant Accident,
report:
- Operability concerns for the residual heat removal pump
- Residual heat removal pumps discharge cross-tie valve
opened vs. closed issue
1991 Westinghouse Report WCAP-12476, Evaluation of LOCA During
Modes 3 and 4 Operation for Westinghouse NSSS, was
submitted to the NRC for approval as a method to resolve the
Modes 3 and 4 loss of coolant accident issue. The analysis
provided by this evaluation was instrumental in many actions
taken by the licensee in regard to Modes 3 and 4 loss of coolant
accident conditions.
January 1992 Station Procedure SYS EJ-120, Placing RHR System in Safety
Injection Standby Condition, was released.
February 1993 Station Procedure OFN BB-031, Shutdown LOCA, was released.
This procedure contained a requirement to cooldown the residual
heat removal system to less than 270°F prior to aligning it in the
injection mode. This was accomplished by increasing component
cooling water flow to the residual heat removal heat exchanger
until residual heat removal temperature was less than 270°F. This
procedure was developed from Abnormal Response Guideline 2,
which was distributed by the Westinghouse Owners Group.
April 1993 Wolf Creek received Westinghouses Nuclear Safety Advisory
Letter NSAL-93-004, RHR Operations as Part of the ECCS
During Plant Startup, dated April 20, 1993, which reiterated the
concern of flashing in the residual heat removal suction line, and
provided an assessment of the safety significance.
Letter NSAL-93-004 also contained recommended actions to
mitigate the condition:
- Assure that the residual heat removal system suction
piping is sufficiently cooled before entering Mode 3
- Force cool the residual heat removal system piping
- Isolate the residual heat removal system from the reactor
coolant system at a low enough temperature at which the
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residual heat removal system pump suction pressure is
above the saturation pressure corresponding to the fluid
temperature
In response Wolf Creek generated Industry Technical Information
Program 02324 to evaluate Letter NSAL-93-004. The purpose of
this evaluation was to ensure the information would receive the
proper technical review and subsequent organizational actions if
required. The stated recommendation of this Industry Technical
Information Program review was to Compare the Westinghouse
recommendations to the operating procedures. Ensure that
adequate guidance was available to preclude the potential for
forming steam voids in the residual heat removal system upon
entry into Mode 3.
June 1993 Following verification that relevant station procedures contained
provisions for forced cooling the residual heat removal suction
piping, operations requested an evaluation of Industry Technical
Information Program 02324 from system engineering to identify
any potential issues that needed to be addressed. (The team
subsequently determined that system engineering had not
evaluated Industry Technical Information Program 02324, safety
analysis instead had performed the evaluation).
August 25, 1993 Engineerings review and evaluation of Industry Technical
Information Program 02324 was completed, and Industry
Technical Information Program 02324 was closed. (Subsequently,
the team determined that the review operations requested by
engineering consisted of a review of the residual heat removal
system piping and instrumentation drawing, a review of relevant
procedures and a teleconference with operations, the industry
technical information program coordinator and engineering.
During this process, operations was asked if the issue of the
Nuclear Safety Advisory Letter had been adequately addressed in
the procedures, and an affirmative reply was received. Based on
this response from operations, the recommendation was that
Industry Technical Information Program 02324 should be closed).
1995 The NRC placed review and approval of Westinghouse
Report WCAP-12476, Evaluation of LOCA During Mode 3 and 4
Operation for Westinghouse NSSS, on hold pending resolution of
the shutdown risk review program.
1999 The Westinghouse Owners Group requested that Westinghouse
Report WCAP-12476, Evaluation of LOCA During Mode 3 and 4
Operation for Westinghouse NSSS, be withdrawn from NRC
review, which was agreed to in 2000.
- 10 - Enclosure
January 18, 2008 Wolf Creek initiated Condition Report 2008-0164, NRC Generic
Letter 2008-001, to address concerns identified in this generic
letter.
March 21, 2008 Wolf Creek initiated Condition Report 2008-000989, Evaluate if
Callaway limitation on RHR suction temperature applies to
WCGS. This condition report was written to evaluate why Wolf
Creek and Callaway treat the Mode 4 alignment of residual heat
removal in shutdown cooling differently.
May 8, 2008 Wolf Creek initiated Condition Report 2008-2187, Draining of B
Residual heat removal Pump. This condition report was written to
document that, while draining the residual heat removal Pump B
and associated suction piping to correct flange leaks on the
residual heat removal Pump B discharge flange and refueling
water storage tank check valve, steam was released into the
room. Initially, the residual heat removal Pump B had been lined
up, and in service, in the shutdown cooling mode providing cooling
to the reactor coolant system. Upon identification of the flange
issue, the pump had been secured, the reactor coolant system
suction isolation valves were shut, and the pump was run on
mini-flow recirculation until pump discharge temperature was
140°F and then the pump was secured. Condition report initiator
postulated: One explanation to getting steam out of the drain line
is that water captured in the line was still at 325°F and flashed to
steam as draining occurred. When the residual heat removal
pump is run in the recirculation mode, there is approximately
15 feet of suction piping that is being recirculated. Upstream of
the recirculation line return is approximately 120 feet of piping that
would not see cooling effect of the recirculation flow. As this hot
water was depressurized, it would turn to steam until the drain was
uncovered and steam allowed to escape. The licensee did not
investigate the reason for steam formation in the residual heat
removal suction piping.
May 10, 2008 Following maintenance to correct flange leaks on the residual heat
removal Pump B discharge flange and refueling water storage
tank check valve, the system was aligned to the reactor coolant
system to retest the affected joints at reactor coolant system
pressure. The pump was secured and the train was subsequently
realigned to take suction from the refueling water storage tank.
The licensee attempted to perform ultrasonic testing of the
residual heat removal piping to check for voids, but found that the
piping was too hot to attach the required instrumentation. The
licensee decided to vent the piping in an effort to reduce
temperature. No condition report was written for this issue.
May 23, 2008 Wolf Creek completed evaluation of Condition Report 2008-0989.
The result of this evaluation stated that the current practice of
using both residual heat removal trains for cooldown was
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acceptable, as allowed by technical specifications and supported
by historical operating experience and Westinghouse
Report WCAP-12476.
August 1, 2008 Wolf Creek initiated Condition Report 2008-3810, Evaluate
potential steam voiding in RHR suction while transitioning to
Mode 3, to address concerns that had been identified during the
review for Generic Letter 2008-01 regarding potential void
formation. This condition report questioned the past operability of
the residual heat removal system when aligned in the injection
mode with suction piping temperature above 260°F as well as the
current design adequacy to ensure cooling of suction piping using
recirculation flow. An evaluation was requested to determine the
effects of potential steam voiding in the residual heat removal
suction piping when realigning the system from reactor coolant
system cooling to emergency core cooling system injection while
transitioning from Mode 4 to Mode 3.
September 23, 2008 Wolf Creek completed their evaluation of Condition
Report 2008-3810. The conclusions that were reached were:
recirculation cannot be relied upon to cool the water in the isolated
suction line, the residual heat removal system would not have
functioned if a loss of coolant accident had occurred in Mode 3,
and the residual heat removal train used for shutdown cooling
should be secured, or put in service, only at a temperature of
240°F to ensure operability.
October 3, 2008 Wolf Creek submitted Licensee Event Report 5000482/2008008-00
in accordance with 10 CFR 50.73.
October 10, 2008 Wolf Creek initiated Condition Report 2008-4997, Missed
opportunity to resolve RHR suction piping issue. This condition
report was initiated to determine why there were different
responses for the same issue in Condition Reports 2008-0989
and 2008-3810. This condition report was also used to perform a
root cause analysis of the potential voiding issue.
December 5, 2008 Wolf Creek completed their evaluation of Condition
Report 2008-004997.
January 30, 2009 Wolf Creek submitted revised Licensee Event
Report 5000482/2008008-01 because further evaluation provided
additional detail to the safety significance and root cause of the
issue.
1.2 Root Cause and Corrective Action Assessment
a. Root Cause Analysis
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The inspectors reviewed and assessed the licensees root cause analysis for technique,
technical accuracy, thoroughness, and corrective actions proposed and taken. The
inspectors reviewed the scope and process used by licensee personnel to identify the
root cause of the potential to have void formation in the suction piping of the residual
heat removal system when transitioning from Mode 4 to Mode 3 with fluid temperatures
above 225°F. The inspectors compared information gained through inspection to the
event information and assumptions made in the root cause analysis. The inspectors
interviewed licensee personnel, reviewed logs, and system design information. The
inspectors also evaluated the licensees extent of condition review.
The licensee entered the potential voiding issue into the corrective action program as
Condition Report 2008-3810, Evaluate Potential Steam Voiding in RHR Suction While
Transitioning to M-3, to address concerns identified during their review of Generic Letter 2008-01 regarding potential void formation in safety-related fluid systems. This
condition report questioned the past operability of the residual heat removal system
when aligned in the injection mode with suction piping temperature above 260°F, as well
as the current design adequacy to ensure cooling of suction piping using recirculation
flow. The licensee classified this as a nonsignificant broke-fix condition report, and an
evaluation was requested to determine the effects of potential steam voiding in the
residual heat removal suction piping when realigning the system from reactor coolant
system cooling to emergency core cooling system injection while transitioning from
Mode 4 to Mode 3. Through this evaluation the licensee determined that:
- If the residual heat removal system is aligned to the emergency core cooling
system injection mode with suction fluid temperature near 350°F, the water in the
suction piping will remain hot for a considerable amount of time. If, while in this
condition, a loss of coolant accident was to occur and the safety injection system
initiated, the residual heat removal pumps would start which would cause
pressure in the suction piping to decrease; and this correlates to a lowering of
the saturation pressure for the corresponding suction piping fluid temperature.
When the suction piping pressure is lowered below the saturation pressure for
the corresponding temperature, this would cause the hot pressurized water to
flash to steam, and as long as the pressure in the suction piping is higher than
the static head of the refueling water storage tank on the supply check valve, the
check valve will not open and no injection flow will occur. This would result in the
steam void continuing to expand and extending to the pump suction and steam
binding the pump.
- Using the mini-flow recirculation line for cooling the suction piping of the residual
heat removal train following alignment for emergency core cooling system
injection can not be relied upon. Specifically, there is approximately 140 feet of
piping upstream of the mini-flow recirculation line, with a significant portion in the
vertical orientation, and this configuration prevents mini-flow recirculation water
from mixing with the stagnant hot water in the suction piping.
- The residual heat removal train should be secured, or put in service, only at a
reactor coolant system temperature of 240°F (including instrument uncertainties).
The licensee subsequently initiated Condition Report 2008-4997, Missed Opportunity to
Resolve RHR Suction Piping Issue, for the purpose of determining why two separate
- 13 - Enclosure
Condition Reports 2008-0989, Evaluate if Callaway Limitation on RHR Suction
Temperature Applies to WCGS; and 2008-3810, Evaluate Potential Steam Voiding in
RHR Suction While Transitioning to M-3; initiated for apparently the same issue came to
different conclusions. This condition report was also used to perform a root cause
analysis of the potential voiding issue associated with the residual heat removal system
as well as a past operability review. Through the evaluations that the licensee
performed, they concluded that:
- From a past operability perspective, the residual heat removal system must be
considered inoperable any time the plant was in Mode 4 with the reactor coolant
system suction isolation valves open and reactor coolant system temperature
was above 249.1°F.
- The residual heat removal system must be considered inoperable in Mode 3
during plant heatup for a period of 46 hours5.324074e-4 days <br />0.0128 hours <br />7.60582e-5 weeks <br />1.7503e-5 months <br /> following isolation from the reactor
coolant system. This is based on the amount of time it would take the suction
piping and fluid to cool down to 225°F.
- From the perspective of past functionality, the residual heat removal system
would not have been functional during a small break loss of coolant accident in
Modes 3 or 4, nor a large break loss of coolant accident in Mode 3 for injection or
recirculation.
Ultimately, through this review the licensee determined that: the direct cause of the
potential voiding issue was that the organization failed to take steps necessary to
preclude voiding in the residual heat removal system and the root cause was the
residual heat removal system design was not adequate to support all three modes of
residual heat removal operation without adversely impacting each other.
The licensee also identified as a contributing cause, for the contradictory findings in the
condition report evaluations, and the missed opportunities to ensure residual heat
removal train operability was the unrecognized complexity of the residual heat removal
systems suction design characteristics which led to a failure by operations and
engineering to perform an adequate evaluation of the impact of hot water in the suction
piping and the affect this had on operability of the residual heat removal pumps. As a
basis for this contributing cause, the licensee identified that the mitigation strategy
chosen to preclude the potential for the flashing of water in the residual heat removal
pump suction line was based on analysis and recommendations provided by
Westinghouse. The strategy chosen (forced cooling using mini-flow recirculation) best fit
the plant system configuration, and Wolf Creek had failed to recognize that the unique
design characteristics of the residual heat removal suction piping created an unanalyzed
condition for flashing in the piping and subsequent voiding in the pump. The design
configuration creates an anomaly in regard to normally accepted standards of water
hammer and flashing criterion. What was not realized was the complexity of the design
configuration dynamics of the suction piping for the residual heat removal system in
regard to flashing and voiding issues. The current technical evaluation performed to
determine residual heat removal operability and the potential impacts of voiding required
extensive research, numerous man-hours, numerous personnel, and assistance from
Westinghouse. This issue is a potential voiding concern with the impact and further
understanding of voiding only recently being recognized.
- 14 - Enclosure
The licensee performed an extent of condition review that examined the challenges in
system operation with respect to maintaining the residual heat removal systems suction
piping sub-cooled. In this review the licensee determined that the direct extent of
condition had been addressed by reviewing the operation of the residual heat removal
system under all plant evolutions and operational modes. Specifically, the licensee
reviewed all evolutions where maintaining the residual heat removal pump suction piping
water sub-cooled could be challenged by changing system dynamics. During this
review, the licensee identified a previously unrecognized concern associated with the
automatic swap-over of residual heat removal pump suction from the refueling water
storage tank to the containment sump in recirculation mode.
The licensee also performed an extent of cause review for the identified root cause.
Through this review, the licensee identified that this operability concern is unique to the
residual heat removal system because of the three functions that this system is called to
perform. Furthermore, the licensee also determined that the other emergency core
cooling system pumps are capable of operating with temperatures of up to 300°F in the
recirculation mode and the design does not indicate susceptibility to the identified cause.
The inspectors determined that the cause evaluation for the potential voiding issue
associated with the residual heat removal system was generally thorough. However, the
inspectors determined that in some areas the root cause analysis was narrowly focused
and lacked technical rigor when evaluating some aspects of the causes of this issue.
Specifically, while the inspectors agreed that system design was a factor in this issue, it
was noted that there was a significant amount of industry information available to the
licensee that both identified the deficient system design and, if appropriately evaluated,
would have identified the specific issue associated with use of the mini-flow recirculation
and its potential system impact.
In particular, Nuclear Safety Advisory Letter NSAL-93-004, RHR Operations as Part of
the ECCS During Plant Startup, dated April 20, 1993, was issued by Westinghouse to
reiterate the concern of flashing in the residual heat removal suction line while in
Modes 3 and 4 operation and provided an assessment of the safety significance. This
advisory described a concern associated with system operation in Mode 4 where the
residual heat removal pumps are lined up and taking suction from the reactor coolant
system then secured, isolated, and realigned to take suction from the refueling water
storage tank prior to transition to Mode 3. In this scenario the pump suction piping and
fluid could be at elevated temperatures (as high as 350°F) for some time after Mode 3 is
entered, and if a safety injection system actuation occurred, and sufficient time had not
elapsed to allow cooling of the system piping by conduction and convection, the pumps
suction pressure could be lowered below the saturation pressure for the corresponding
temperature. This would result in fluid in the suction piping flashing to steam and
potentially rendering the system inoperable. The inspectors noted that Nuclear Safety
Advisory Letter NSAL-93-004 also contained recommended actions to mitigate the
condition:
- Assure that the residual heat removal system suction piping is sufficiently cooled
before entering Mode 3
- Force cool the residual heat removal system piping
- 15 - Enclosure
- Isolate the residual heat removal system from the reactor coolant system at a low
enough temperature at which the residual heat removal system pump suction
pressure is above the saturation pressure corresponding to the fluid temperature
However, the advisory specifically identified in the technical evaluation section that use
of the mini-flow recirculation method force cools the piping downstream of the mini-flow
return and only provides cooling of the water upstream of the mini-flow connection by
means of conduction and convection.
As such, the inspectors determined that inadequate engineering evaluations, which had
been performed by the licensee, both historically and recently, was another cause of this
issue. Of note, the inspectors identified that the licensee has an ongoing engineering
improvement plan from other similar issues associated with engineering rigor, which was
still in process at the end of the inspection and tracking the completion of this initiative
was credited by the licensee as the corrective action for the contributing cause.
Also, the inspectors considered the evaluation to be narrowly focused and lacking in
technical rigor with respect to the extent of condition review. Specifically, during their
review, the inspectors noted that Station Procedure AP 28A-100, Section 4.5.1,
Revision 7, "Condition Reports, extent of condition is defined as, The extent to which
the actual condition exists or can exist in other plant processes, equipment or human
performance. The objective is to reasonably bound the condition in regards to the
relative risk it creates for the station. Accordingly, the inspectors determined that the
extent of condition review performed by the licensee was narrowly focused on only the
residual heat removal system, and as such, was not a true extent of condition as defined
by the station procedure.
b. Corrective Actions
The inspectors evaluated the scope, adequacy, and timeliness of the licensees
corrective measures that were both planned and implemented in response to the
potential steam voiding issue associated with the residual heat removal system. The
inspectors concluded that the actions both planned and implemented by the licensee
were appropriate to address the identified issue, to prevent recurrence, and were
consistent with the safety significance of the issue. These corrective actions included:
- Issuing essential reading to the operational crews to keep them aware of the
operational changes to the residual heat removal system in Modes 3 and 4
- Issuing operating experience to the industry detailing the concern with the
residual heat removal system in Modes 3 and 4
- Revising station calculations to preclude steam voiding
- Revising station operating procedures to only use one train of residual heat
removal for reactor coolant system temperature control and to also disable the
auto swap-over feature for the train that is used prior to initiation of shutdown
cooling.
- 16 - Enclosure
1.3 Related Operating Experience
The team noted that that there was a significant amount of applicable industry
information available to the licensee that identified the deficient system design as well as
identifying the specific issue associated with use of the mini-flow recirculation and its
potential system impact. However, inadequate evaluation of this information resulted in
inappropriate implementation of actions by the station.
The team determined the licensees Industry Operating Experience Program previously
lacked rigor when evaluating industry operating experience and its applicability to the
facility. Specifically, the licensee performed an inadequate evaluation of Nuclear Safety
Advisory Letter 93-004, RHRS Operation as Part of the ECCS During Plant Startup.
The team determined that significant improvements have been made to the stations
program and procedures pertaining to assessing industry operating experience.
Specifically, the licensee has enhanced the following:
- The initial screening determines if the document could potentially impact the
safety or reliability of Wolf Creek Generating Station and insures that the
document is entered in the Corrective Action Program.
- The Supervisor of Improvement Program shall ensure the periodic (at least once
per 18 months) performance of effectiveness reviews monitor the success of the
Industry Operating Experience Program in attaining its desired objectives and
improvements.
- The first significant operating experience effectiveness review is to be performed
one year after completion of all corrective and preventative actions and each
subsequent effectiveness review is to be scheduled every 24 months thereafter.
- A significant operating experience effectiveness review shall be completed on all
identified recommendations every six years.
The team noted that the licensee had performed an Industry Operating Experience
Re-Evaluation Project to resolve the extent of condition and extent of cause in the quality
of evaluations between January 1, 2003, and July 31, 2008. This was performed due to
Corrective Action 4543 from Condition Report 2008-000717. The project consisted of
reviewing a sample of 104 from a total of 451 evaluations with an acceptance standard
of four or less defective evaluations. The definition of a defective evaluation is when the
entire product is considered unacceptable. An evaluation team, which consisted of
maintenance, operations, licensing, engineering, and operating experience personnel,
identified eight defective evaluations. Subsequently, an expert panel consisting of a
manager of Regulatory Affairs, supervisor of root cause/corrective action, and supervisor
of operations reviewed the eight defectives and the definition of defective, and
concluded that only four of the eight operating experience evaluations met the defective
definition. Thus, four defective evaluations were identified in the project; therefore,the
licensee concluded that no extent of condition or extent of cause was needed.
The team did not review current station evaluations of industry operating experience;
however, the team reviewed the four operating experience evaluations that were
screened out by the expert panel during the Industry Operating Experience
- 17 - Enclosure
Re-Evaluation Project. Subsequently, the inspectors identified a recent industry
operating experience evaluation, as documented in Condition Report 2007-2656, which
was completed in December 2008. This condition report was written to evaluate
Information Notice 2007-01, Recent OE Concerning Hydrostatic Barriers. The
evaluation section of the condition report takes credit for a corrective action associated
with Condition Report 2008-3745. When the inspectors reviewed this condition report, it
was determined that this corrective action did not address all aspects which were
identified in Information Notice 2007-01. Therefore, the team questioned the evaluation
done in Condition Report 2007-2656. The licensee was informed of the teams questions
and subsequently the licensees corrective action, licensing, and operating experience
personnel reviewed and determined that the evaluation of the Information
Notice 2007-01 in Condition Report 2007-2656 was inadequate and wrote Condition
Report 2009-000939 to address this concern.
1.4 Potential Generic Issues
The team evaluated the circumstances associated with the potential voiding issue and
assessed the root cause analysis. Along with this, the team interviewed numerous
licensee personnel and reviewed industry operating experience, evaluations the station
had performed to analyze this issue as well as NRC generic communications with the
goal of identifying any potentially generic issues that should be addressed as a result of
this event.
The team concluded that, while there is a potential for voiding to occur in any fluid
system at any facility, there are no potentially previously unrecognized generic concerns
associated with this issue. The team also noted that the licensee has issued an
operating experience report to the industry for future reference.
1.5 Event Precursors
The team performed a review of the licensees corrective action program documents
associated with the residual heat removal system as well as conducting interviews with
station personnel to determine if any previous issues associated with the system could
have been viewed as event precursors to the potential voiding condition identified by the
licensee. During this review, the team considered previously encountered issues where
steam voiding was identified in the suction piping of the residual heat removal system.
The inspectors identified two previous events, which had not been recognized by the
licensee in their evaluation, that were indicative of the potential voiding issue.
Specifically:
- On May 8, 2008, Wolf Creek initiated Condition Report 2008-2187, Draining of
B RHR Pump, to document that, while attempting to drain the residual heat
removal Pump B and associated suction piping to allow performance of
corrective maintenance, steam was released into the room that resulted in a
personnel contamination event. This condition report established that, prior to
the draining evolution of the residual heat removable, Pump B had been in
service providing cooling the reactor coolant system in the shutdown cooling
mode. In preparation for the maintenance, the pump had been secured in
accordance with Station Procedure SYS EJ-321, Revision 7, Shut Down of a
Residual heat removal Train, of which step 6.2.3 required that the pump be run
- 18 - Enclosure
in the recirculation mode until the discharge temperature indicates less than
270°F (the licensee ran the pump in this mode until the discharge temperature
indicated 140°F and then secured the pump). Then licensee personnel began
draining the pump and piping. Initially, water issued from the pipe but then steam
began to issue from the piping which caused the tubing to come out of the floor
drain and an individual was contaminated. The condition report initiator
postulated in the condition description of the condition report that: One
explanation to getting steam out of the drain line is that water captured in the line
was still at 325 degrees and flashed to steam as draining occurred. When the
residual heat removal pump is run in the recirculation mode, there is
approximately 15 feet of suction piping that is being recirculated. Upstream of
the recirculation line return is approximately 120 feet of piping that would not see
cooling effect of the recirculation flow. As this hot water was depressurized, it
would turn to steam until the drain was uncovered and steam allowed to escape.
However, the licensee did not investigate the reason for steam formation in the
residual heat removal suction piping; instead the focus of this condition report
was to determine a better method to secure the drain hoses.
- On May 10, 2008, following maintenance to correct flange leaks on the residual
heat removal Pump B discharge flange and refueling water storage tank check
valve, the system was aligned to the reactor coolant system, as part of the retest,
to place reactor coolant system pressure on the affected joints. Subsequently,
the pump was secured and the train was realigned to take suction from the
refueling water storage tank. At this point the licensee attempted to perform
ultrasonic testing of the residual heat removal piping to check for voids, but found
that the piping was too hot to attach the required instrumentation. The licensee
decided to vent the piping in an effort to reduce temperature and vented a mixture
of steam and water for approximately 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> before the suction piping became
water solid. Though the team noted that there was some discussion and
consideration of operability, they determined that the methods and assumptions
being used were determined to not be valid. Therefore, it is uncertain if the
system would have functioned properly if needed. The licensee did not
investigate this issue any further, nor did they enter this into their corrective action
program.
Based on this, the team determined that there had been recent event precursors
documented by the licensee in various facility databases. As such, the team
concluded that due to the lack of a questioning attitude, the licensee had failed to
recognize and/or thoroughly evaluate the underlying condition associated with
why steam was vented from the residual heat removal system when it was not
expected based on system conditions. As such, this lack of questioning attitude
resulted in the licensees failure to recognize and analyze pertinent information
associated with prior issues which were precursors to the issue identified on
August 1, 2008.
1.6 Reportability Review
The licensee evaluated the potential voiding condition associated with the residual heat
removal system and determined that this was reportable to the NRC in accordance with
10 CFR 50.73(a)(2)(i)(B) as a 60-day report because it represented an operation or
condition prohibited by technical specifications at the station. As such, Licensee Event
- 19 - Enclosure
Report 05000482/2008008-00 was submitted on October 3, 2008. This report contained
a summary of the initial information known by the licensee at the time of submission.
Further evaluation conducted by the licensee provided additional details relative to the
safety significance of this issue as well as determining the root cause of the event and
past operability of the system. Accordingly, the licensee submitted revised Licensee
Event Report 05000/2008008-01 on January 1, 2009.
The team reviewed the licensee event reports and determined that the identified aspects
of the licensees reportability determination were correct. However, while reviewing the
licensees past operability determination contained in the root cause analysis, the team
noted the following conclusions:
- From a past operability perspective, the residual heat removal system must be
considered inoperable any time the plant was in Mode 4 with the reactor coolant
system suction isolation valves open and reactor coolant system temperature
was above 249.1°F.
- The residual heat removal system must be considered inoperable in Mode 3
during plant heatup for a period of 46 hours5.324074e-4 days <br />0.0128 hours <br />7.60582e-5 weeks <br />1.7503e-5 months <br /> following isolation from the reactor
coolant system. This is based on the amount of time it would take the suction
piping and fluid to cool down to 225°F.
- From the perspective of past functionality, the residual heat removal system
would not have been functional during a small break loss of coolant accident in
Modes 3 or 4, nor a large break loss of coolant accident in Mode 3 for injection or
recirculation.
Based on this and information contained in the licensees root cause analysis, the team
determined that on March 20, 2008, while in Mode 4 performing a plant cool down for
Refueling Outage 16, the licensee had operated the residual heat removal system in a
condition prohibited by technical specifications. The team also determined that the
licensees operation of the residual heat removal system on March 20, 2008 and on May
10, 2008, resulted in a condition that prevented the residual heat removal system from
performing its safety function. As such, the team noted that the revised Licensee Event
Report 05000/2008008-01 did not identify these reportable conditions, nor had the
licensee submitted a separate licensee event report to inform the NRC of the instances
that had been identified. Therefore, the team concluded that the licensee had failed to
report instances where the residual heat removal system was operated in a condition
prohibited by technical specifications, and a loss of safety function of the system existed
between March 20, 2008 and December 8, 2008.
The team informed the licensee of their concern. The licensee subsequently entered
this into their corrective action program as Condition Reports 2009-1261, and 2009-1326
and Action Requests 15244, 17776, and 15306.
The team determined that the licensees failure to properly report when the station was
operated in a condition prohibited by technical specifications and there was a loss of
safety function of the residual heat removal system was a violation of 10 CFR 50.73,
Licensee Event Report System. Details associated with this violation are described in
Section 2.1 of this report.
- 20 - Enclosure
2.0 Focused Baseline Inspection Findings
2.1 Failure to Report Conditions Prohibited By Technical Specifications
Introduction. The inspectors identified a Severity Level IV noncited violation of 10 CFR
50.73 for failure to submit a licensee event report within 60 days following discovery of
an event meeting the reportability criteria.
Description. On September 23, 2008, the licensee completed an evaluation of a
potential steam voiding issue associated with the residual heat removal systems suction
piping that could occur when transitioning from Mode 4 to Mode 3 with elevated fluid
temperatures. Based on the results of this evaluation, the licensee determined that both
trains of the residual heat removal system had been inoperable during the startup from
Refueling Outage 16, on May 10, 2008. Specifically, the residual heat removal system
would not have functioned if a loss of coolant accident had occurred in Mode 3 due to
elevated suction piping fluid temperature following transition to Mode 3 from Mode 4. As
a result, on October 3, 2008, the licensee submitted Licensee Event
Report 05000482/2008008-00, in accordance with 10 CFR 50.73(a)(2(i)(B), to report an
operation or condition prohibited by plant technical specifications.
Based on further evaluation conducted by the licensee, additional details relative to the
safety significance of the potential steam voiding issue and past operability of the
residual heat removal system were identified. Accordingly, the licensee submitted
revised Licensee Event Report 05000/2008008-01 on January 1, 2009, to provide the
NRC with this additional information that had been learned relative to the residual heat
removal systems operation on May 10, 2009.
The inspectors reviewed the licensee event reports that had been submitted to the NRC.
During this review, the inspectors determined that the licensee had correctly identified
and evaluated a reportability aspect during their review. However, while reviewing the
licensees past operability determination contained in the root cause analysis, the
inspectors noted the following conclusions:
- From a past operability perspective, the residual heat removal system must be
considered inoperable any time the plant was in Mode 4 with the reactor coolant
system suction isolation valves open and reactor coolant system temperature
was above 249.1°F.
- The residual heat removal system must be considered inoperable in Mode 3
during plant heatup for a period of 46 hours5.324074e-4 days <br />0.0128 hours <br />7.60582e-5 weeks <br />1.7503e-5 months <br /> following isolation from the reactor
coolant system. This is based on the amount of time it would take the suction
piping and fluid to cool down to 225°F.
- From the perspective of past functionality, the residual heat removal system
would not have been functional during a small break loss of coolant accident in
Modes 3 or 4, nor a large break loss of coolant accident in Mode 3 for injection or
recirculation.
Based on this and information contained in the licensees root cause analysis, the
inspectors determined that on March 20, 2008, while in Mode 4 performing a plant cool
down for Refueling Outage 16, the licensee had operated the residual heat removal
- 21 - Enclosure
system in a condition prohibited by technical specifications as well. The inspectors also
determined that the licensees operation of the residual heat removal system on
March 20, 2008, and on May 10, 2008, resulted in a condition that prevented the
residual heat removal system from performing its safety function. As such, the
inspectors noted that both of these issues were reportable as defined by 10 CFR 50.73,
and the revised Licensee Event Report 05000/2008008-01 did not identify these
reportable conditions, nor had the licensee submitted a separate licensee event report to
inform the NRC of the instances that had been identified. Therefore, the inspectors
concluded that the licensee had failed to report instances where the residual heat
removal system had been operated in a condition prohibited by technical specifications
and a loss of safety function of the system existed between March 20, 2008, and
December 8, 2008.
The inspectors informed the licensee of their concerns. The licensee initiated Condition
Report 2009-1261 and Action Requests 15244, 17776, and 15306 to address this
concern.
Analysis. The inspectors reviewed this issue in accordance with Inspection Manual
Chapter 0612 and the NRC Enforcement Manual. Through this review, the inspectors
determined that traditional enforcement was applicable to this issue because the NRC's
regulatory ability was affected. Specifically, the NRC relies on licensee to identify and
report conditions or events meeting the criteria specified in regulations in order to
perform its regulatory function, and when this is not done, the regulatory function is
impacted. The inspectors determined that this finding was not suitable for evaluation
using the significance determination process, and as such, was evaluated in accordance
with the NRC Enforcement Policy. The finding was reviewed by NRC management and
because the violation was determined to be of very low safety significance, was not
repetitive or willful, and was entered into the corrective action program, this violation is
being treated as a Severity Level IV noncited violation consistent with the NRC
Enforcement Policy. This finding was determined to have a crosscutting aspect in the
area of Problem Identification and Resolution associated with the corrective action
program P.1(c), in that the licensee failed to appropriately and thoroughly evaluate for
reportability aspects all factors and time frames associated with the inoperability of
residual heat removal system when suction temperatures were above 249°F.
Enforcement. Title 10 CFR 50.73(a)(1) requires, in part, that licensees shall submit a
licensee event report for any event of the type described in this paragraph within 60 days
after the discovery of the event. Title 10 CFR 50.73(a)(2)(i)(B) requires, in part, that the
licensee report any operation or condition prohibited by the plant's technical
specification. Contrary to the above, it was determined that the residual heat removal
system had been operated in a condition prohibited by technical specifications during the
cool down for Refueling Outage 16 on March 20, 2008; and the licensee failed to submit
a licensee event report or include this information in revised Licensee Event
Report 05000482/2008008-01, submitted on January 1, 2009. This finding was
determined to be applicable to traditional enforcement because the failure to report
conditions or events meeting the criteria specified in regulations affects the NRCs
regulatory ability. The finding was evaluated in accordance with the NRC's Enforcement
Policy. The finding was reviewed by NRC management and because the violation was
of very low safety significance, was not repetitive or willful, and was entered into the
corrective action program, this violation is being treated as a Severity Level IV noncited
violation, consistent with the NRC Enforcement Policy: NCV 05000482/2009006-01,
- 22 - Enclosure
Failure to Report Conditions Prohibited by Technical Specifications, and Safety System
Functional Failures.
2.2 Inadequate Procedures for Mode Shifting of the Residual Heat Removal System
Introduction. The inspectors identified a noncited violation of Technical Specification 5.4.1, Procedures, associated with the licensees failure to ensure that adequate
procedures were available for changing modes of operation of the residual heat removal
system from shutdown cooling to emergency core cooling system operation.
Description. On January 18, 2008, the licensee initiated Condition Report 2008-0164 to
address NRC Generic Letter 2008-001, Managing Gas Accumulation in Emergency
Core Cooling, Decay Heat Removal, and Containment Spray Systems, concerns. The
purpose of this condition report was to evaluate the licensing basis, design, testing, and
corrective action programs for the emergency core cooling systems, residual heat
removal system, and containment spray system to ensure that gas accumulation is
maintained less than the amount that challenges operability of these systems, and that
appropriate action is taken when conditions adverse to quality are identified.
On May 10, 2008, following maintenance to correct flange leaks on the residual heat
removal Pump B discharge flange and refueling water storage tank check valve, the
system was aligned to the reactor coolant system, as part of the retest, to place reactor
coolant system pressure on the affected joints. Subsequently, the pump was secured
and the train was realigned to take suction from the refueling water storage tank. At this
point, the licensee attempted to perform ultrasonic testing of the residual heat removal
piping to check for voids, but found that the piping was too hot to attach the required
instrumentation. The licensee decided to vent the piping in an effort to reduce
temperature and vented a mixture of steam and water for approximately 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> before
the suction piping became water solid. The licensee initiated Station Work
Order 08-306203-000 to perform troubleshooting to determine if the suction piping
temperature was below saturation temperature where the recirculation line taps into the
system.
Subsequently, during the stations evaluation of Condition Report 2008-0164, an
operations representative identified a concern with the potential for steam binding.
Specifically, steam voiding concerns that had been identified during restoration of the
residual heat removal system at the end of Refueling Outage 16, on May 10, 2008,
which could happen any time the station enters Mode 3, combined with the findings from
the generic letter review, prompted the initiation of another condition report to review
these concerns.
On August 1, 2008, station personnel initiated Condition Report 2008-3810 to address
concerns that had been identified during the review for Generic Letter 2008-01 regarding
potential void formation. This condition report questioned the past operability of the
residual heat removal system when aligned in the injection mode with suction piping
temperature as high as 350°F, as well as the current design adequacy to ensure cooling
of suction piping using the mini-flow recirculation line. An evaluation was requested to
determine the effects of potential steam voiding in the residual heat removal suction
piping when realigning the system from reactor coolant system cooling to emergency
core cooling system injection while transitioning from Mode 4 to Mode 3.
- 23 - Enclosure
On September 23, 2008, the licensee completed their evaluation of the potential voiding
issue and concluded that recirculation can not be relied upon to cool the water in the
isolated suction line, the residual heat removal system would not have functioned if a
loss of coolant accident had occurred in Mode 3 with elevated suction piping fluid
temperature, and the residual heat removal train used for shutdown cooling should be
secured, or put in service, only at a temperature of 240°F to ensure operability.
On October 10, 2008, the licensee initiated Condition Report 2008-4997, Missed
Opportunity to Resolve RHR Suction Piping Issue, for the purpose of determining why
two separate conditions initiated for apparently the same issue came to different
conclusions. This condition report was also used to perform a root cause analysis of the
potential voiding issue associated with the residual heat removal system as well as
performing a past operability review.
On December 5, 2008, the licensee completed their evaluations as directed by Condition
Report 2008-4997. Through the evaluations that the licensee performed, they
concluded that:
- From a past operability perspective, the residual heat removal system must be
considered inoperable any time the plant was in Mode 4 with the reactor coolant
system suction isolation valves open and reactor coolant system temperature
was above 249.1°F.
- The residual heat removal system must be considered inoperable in Mode 3
during plant heatup for a period of 46 hours5.324074e-4 days <br />0.0128 hours <br />7.60582e-5 weeks <br />1.7503e-5 months <br /> following isolation from the reactor
coolant system. This is based on the amount of time it would take the suction
piping and fluid to cool down to 225°F.
- From the perspective of past functionality, the residual heat removal system
would not have been functional during a small break loss of coolant accident in
Modes 3 or 4, nor a large break loss of coolant accident in Mode 3 for injection or
recirculation.
Ultimately, through this review, the licensee determined that the direct cause of the
potential voiding issue was that the organization failed to take steps necessary to
preclude voiding in the residual heat removal system and the root cause was the
residual heat removal system design was not adequate to support all three modes of
residual heat removal operation without adversely impacting each other. The licensee
also identified as a contributing cause, for the contradictory findings in the condition
report evaluations and the missed opportunities to ensure residual heat removal train
operability was the unrecognized complexity of the residual heat removal systems
suction design characteristics which led to a failure by operations and engineering to
perform an adequate evaluation of the impact of hot water in the suction piping and the
affect this had on operability of the residual heat removal pumps.
The inspectors reviewed the licensees root cause analysis for this issue. While the
inspectors agreed that system design was a factor in this issue, they however noted that
there was a significant amount of industry information available to the licensee that both
identified the deficient system design and, if appropriately evaluated, would have
identified the specific issue associated with use of the mini-flow recirculation and its
potential system impact. As such, the inspectors determined that engineering
- 24 - Enclosure
evaluations, which had been performed by the licensee, both historically and recently,
was another cause of this issue. Of note, the inspectors identified that the licensee has
an ongoing engineering improvement plan from other similar issues associated with
engineering rigor, which is still in process and tracking the completion of this initiative
was credited by the licensee as the corrective action for the contributing cause.
Analysis. The licensees failure to ensure that adequate procedures were available for
changing modes of operation of the residual heat removal system from shutdown cooling
to emergency core cooling system operation was a performance deficiency. The finding
was more than minor because it was associated with the equipment performance
attribute of the Mitigating Systems Cornerstone and it directly affected the cornerstone
objective to ensure the availability, reliability, and capability of systems that respond to
initiating events to prevent undesirable consequences. Using Inspection Manual
Chapter 0609, Significance Determination Process, Phase 1 Worksheet, the inspectors
concluded that a Phase 2 evaluation was required because this finding represented a
loss of safety function of the residual heat removal system.
The inspectors performed a Phase 2 analysis using Appendix A, Determining the Safety
Significance of Reactor Inspection Findings for At-Power Situations, of Inspection
Manual Chapter 0609, Significance Determination Process, and the plant specific
Phase 2 presolved tables and worksheets for Wolf Creek. The inspectors determined
that the Phase 2 presolved tables and worksheets did not contain appropriate target sets
to accurately estimate the risk input of the finding. Therefore, it was determined that a
Phase 3 analysis was required.
Senior risk analysts performed a Phase 3 analysis of this issue. The estimated
Conditional Core Damage Probability was determined to be 2.84E-7, and the estimated
Conditional Large Early Release Probability was determined to be 2.72E-9. Based on
these results, the finding was determined to be of very low safety significance, Green.
The complete Phase 3 analysis is available from the Publicly Available Records
component of NRCs document systems (ADAMS) as ML091760764.
This finding was determined to have a crosscutting aspect in the area of Problem
Identification and Resolution associated with the corrective action program P.1(c), in
that the licensee failed to appropriately and thoroughly evaluate problems such that the
resolutions address the causes.
Enforcement. Technical Specifications, Section 5.4.1, Procedures, requires, in part,
that written procedures shall be established, implemented, and maintained covering the
applicable procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A,
dated February 1978. Regulatory Guide 1.33, Appendix A, Section 3.c, requires, in part,
that instructions for changing modes of operation of the residual heat removal system
should be prepared. Contrary to the above from 1992 through December 2008, the
licensee failed to provide adequate instructions for changing modes of operation of the
residual heat removal system. Specifically, station procedures allowed the residual heat
removal system to be realigned to the emergency core cooling system mode of
operation when the system was not able to perform its safety function. Because this
violation was of very low safety significance and it was entered into the licensees
corrective action program as Condition Reports 2008-3810 and 2008-4997, this violation
- 25 - Enclosure
is being treated as a noncited violation, consistent with Section VI.A of the NRC
Enforcement Policy: NCV 05000482/2009006-02, Inadequate Instructions for Changing
Modes of Operation of the Residual Heat Removal System.
4OA6 Meetings
Exit Meeting Summary
On February 27, 2009, prior to the teams departure from the facility, an inspection debrief was
conducted with Mr. R.A. Muench, President and CEO, and other members of the licensee staff
to apprise them of the teams results to date and to explain that the inspection would continue
with in office review pending resolution of all questions.
On July 9, 2009, the team conducted a telephonic exit meeting to present the inspection results
to Mr. Matt Sunseri, Vice President of Operations and Plant Manager, and other members of the
licensee staff. The licensee acknowledged the issues presented. The team acknowledged
review of proprietary material, as part of the inspection but no proprietary information was
included in the report.
- 26 - Enclosure
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee Personnel
R. Muench, President and Chief Executive Officer
M. Sunseri, Vice President Operations and Plant Manager
S. Hedges, Vice President Oversight
G. Pendergrass, Manager, System Engineering
T. Garrett, Vice President Engineering
G. Neisis, Manager Design
S. Henry, Manager Operations
R. Flannigan, Manager Regulatory Affairs
D. Hooper, Supervisor Licensing
W. Muilenburg, Licensing
J. Hsen, Safety Analysis
D. Erbe, Manager Security
S. Skidmore, Corrective Actions
F. Laflin, Chief Engineer
J. Patel, Engineering Supervisor
W. Ketchum, Supervisor Fuels/Probabilistic Safety Analysis
L. Parmenter, Assistant to Operations Manager
T. Card, Supervisor System NSSS
S. Koenig, Manager Corrective Actions
J. Harris, System Engineer
D. Garrison, Operations Support
NRC Personnel
J. Josey, Resident Inspector
M. Young, Reactor Inspector
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened and Closed
05000482/2009006-01 NCV Failure to Report Conditions Prohibited by Technical
Specifications and Safety System Functional Failures05000482/2009006-02 NCV Inadequate Instructions for Changing Modes of Operation
of the Residual Heat Removal System
Closed
None
A-1 Attachment
LIST OF DOCUMENTS REVIEWED
PROCEDURES
NUMBER TITLE REVISION
SYS BG-216 Reactor Make-up Control System Alternate 24
Operation
EMG C-11 Loss of Emergency Coolant Recirculation 20
EDMG-T01 EDMG Tool Box 4
EMG C-13 Control Room Response to Sump Blockage 2
OFN EJ-015 Loss of RHR Cooling 15A
SYS EJ-121 Startup of a RHR Train in Cooldown Mode 21
SYS EJ-120 Startup of a Residual Heat Removal Train 51
GEN 00-006 Hot Standby to Cold Shutdown 68
GEN 00-008 Reduced Inventory Operations 18A
AP 20E-001 Industry Operating Experience Program 12
AP 28A-100 Condition Reports 7
OFN EJ-40 CL Recirc During Mode 3, With Accumulators 2
Isolated, Mode 4, 5 or 6
EMG ES-11 Post LOCA Cooldown and Depressurization 14
EMG ES-12 Transfer to Cold Leg Recirculation 12
GEN 00-002 Cold Shutdown to Hot Standby 67A
SYS EJ-320 Placing RHR System In Safety Injection Standby 32
Condition
EP-01-2.1-1 Emergency Action Levels 10
EPP 01-2.1 Emergency Classification 18
OFN BB-031 Shutdown LOCA 9
STS EJ-100A RHR System Inservice Pump A Test 23
STS EJ-100B RHR System Inservice Pump B Test 19
SYS EJ-321 Shutdown of a Residual Heat Removal Train 23
SYS EJ-323 RHR System Depressurization 9
OFN NB-34 Loss of All AC Power - Shutdown Conditions 5
ALAR 00-050C RHR Loop 2 Flow Lo 10
ALAR 00-49C RHR Loop 2 Flow Lo 11
A-2 Attachment
CALCULATIONS
NUMBER TITLE REVISION
AN-01-025 No Title 0
AN-97-027 Time To Boil In The Core and Core Uncovery In 0
The Event of a Loss of RHR Cooling During
Refueling 9
CONDITION REPORTS
2007-2162 2008-2187 2008-2262 2008-4997 2008-5917
2007-2656 2008-0717 2008-3745 2008-5912 2009-0939
2008-0164 2008-0989 2008-3810 2008-5913 2009-1261
2008-0717 2008-2187 2008-4997 2008-5915
2008-0989
PERFORMANCE IMPROVEMENT REQUEST
MISCELLANOUS
NUMBER TITLE REVISION
NSAL-93-004 RHRS Operation as Part of the ECCS During Plant 0
Startup
LER 2008-008-00 Potential for Residual Heat Removal Trains to be 0
Inoperable during Mode Change
LER 2008-008-00 Potential for Residual Heat Removal Trains to be 1
Inoperable during Mode Change
ITIP 02324 Westinghouse Letter SAP-93-706 (4-29-93): RHR 0
Operation As Part Of The ECCS During Plant
Startup (Residual Heat Removal) (NSAL-93-004)
ITIP 05342 Westinghouse InfoGram IG-04-6: Reactor Trip February 25,
Breaker Auto Shunt Trip Test Panel. 2009
ITIP 05288 SER 3-04 - Reactor Overpower Events Associated February 25,
with Ultrasonic Feedwater Flow Measurement 2009
Systems
SEL 2009-135 Self Assessment Plan Industry Operating
Experience Program
Assessment 92 Assessment/Audit Detail Report Industry Operating September 21,
Experience Program 2007
A-3 Attachment
NUMBER TITLE REVISION
Quick Hit Detail Report IOE Re-Evaluation Project
1369
LTR-LIS-09-361 Engineering Report Wolf Creek Generating Station June 5, 2009
Modes 3 and 4 Loss-of-Coolant Accident Analysis
For Residual Heat Removal Operability Study
SY1300600 Emergency Core Cooling System 18
SY1300500 Residual Heat Removal 15
SY1505900 Feedwater System 16
SY1303200 Containment System 15
SY1300600 Emergency Core Cooling System 18
SY1300400 Chemical Volume and Control System 22
A-4 Attachment