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| issue date = 08/13/2013
| issue date = 08/13/2013
| title = IR 05000220-13-003, 05000410-13-003; on 04/01/2013 - 06/30/2013; Nine Mile Point Nuclear Station (NMPNS) Units 1 and 2; Surveillance Testing, Problem Identification and Resolution, Follow-Up of Events and Notices of Enforcement Discretion
| title = IR 05000220-13-003, 05000410-13-003; on 04/01/2013 - 06/30/2013; Nine Mile Point Nuclear Station (NMPNS) Units 1 and 2; Surveillance Testing, Problem Identification and Resolution, Follow-Up of Events and Notices of Enforcement Discretion
| author name = Schroeder D L
| author name = Schroeder D
| author affiliation = NRC/RGN-I/DRP/PB1
| author affiliation = NRC/RGN-I/DRP/PB1
| addressee name = Costanzo C
| addressee name = Costanzo C
Line 9: Line 9:
| docket = 05000220, 05000410
| docket = 05000220, 05000410
| license number = DPR-063, NPF-069
| license number = DPR-063, NPF-069
| contact person = Schroeder D L
| contact person = Schroeder D
| document report number = IR-13-003
| document report number = IR-13-003
| document type = Inspection Report, Letter
| document type = Inspection Report, Letter
| page count = 73
| page count = 73
}}
}}
See also: [[followed by::IR 05000220/2013003]]
See also: [[see also::IR 05000220/2013003]]


=Text=
=Text=
{{#Wiki_filter:UNITED STATES                         NUCLEAR REGULATORY COMMISSION                                                         REGION I                           2100 RENAISSANCE BOULEVARD, SUITE 100                         KING OF PRUSSIA, PENNSYLVANIA 19406-2713
{{#Wiki_filter:UNITED STATES
August 13, 2013  
                                NUCLEAR REGULATORY COMMISSION
  Mr. Christopher Costanzo, Vice President Nine Mile Point Nuclear Station Constellation Energy Nuclear Group, LLC P.O. Box 63  
                                                REGION I
                                2100 RENAISSANCE BOULEVARD, SUITE 100
                              KING OF PRUSSIA, PENNSYLVANIA 19406-2713
                                            August 13, 2013
Mr. Christopher Costanzo, Vice President
Nine Mile Point Nuclear Station
Constellation Energy Nuclear Group, LLC
P.O. Box 63
Lycoming, NY 13093
SUBJECT:        NINE MILE POINT NUCLEAR STATION - NRC INTEGRATED INSPECTION
                REPORT 05000220/2013003 AND 05000410/2013003
Dear Mr. Costanzo:
On June 30, 2013, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at
your Nine Mile Point Nuclear Station (NMPNS) Units 1 and 2. The enclosed inspection report
documents the inspection results, which were discussed on July 25, 2013, with you and other
members of your staff.
The inspection examined activities conducted under your license as they relate to safety and
compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed
personnel.
This report documents one self-revealing apparent violation concerning the improper restoration
of a direct current electrical bus which resulted in a loss of all shutdown cooling. The safety
significance of the violation is still under review pending the outcome of a Phase III risk analysis
by NRC Senior Reactor Analysts. However, the violation does not represent an immediate
safety concern because Constellation has conducted a prompt human performance event
review, entered the issue into their corrective action program (CAP), and conducted a root
cause analysis. Additionally, corrective actions including a review of all emergency, off-normal,
and normal system operating procedures are in progress. This violation with the supporting
circumstances and details is documented in this inspection report.
This report documents two NRC-identified findings and two self-revealing findings of very low
safety significance (Green). These findings were determined to involve violations of NRC
requirements. However, because of the very low safety significance, and because they are
entered into your CAP, the NRC is treating these findings as non-cited violations (NCVs)
consistent with Section 2.3.2 of the NRC Enforcement Policy. If you contest any NCVs in this
report, you should provide a response within 30 days of the date of this inspection report with
the basis of your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control
Desk, Washington D.C. 20555-0001; with copies to the Regional Administrator, Region I; the
Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, D.C.
20555-0001; and the NRC Resident Inspector at NMPNS. In addition, if you disagree with the


Lycoming, NY 13093
C. Costanzo                                        2
cross-cutting aspect assigned to any finding in this report, you should provide a response within
30 days of the date of this inspection report, with the basis for your disagreement, to the
Regional Administrator, Region I, and the NRC Resident Inspector at NMPNS.
In accordance with Title 10 of the Code of Federal Regulations 2.390 of the NRCs Rules of
Practice, a copy of this letter, its enclosure, and your response (if any) will be available
electronically for public inspection in the NRC Public Document Room or from the Publicly
Available Records component of the NRCs Agencywide Documents Access Management
System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-
rm/adams.html (the Public Electronic Reading Room).
                                                Sincerely,
                                                /RA/
                                                Daniel L. Schroeder, Chief
                                                Reactor Projects Branch 1
                                                Division of Reactor Projects
Docket Nos: 50-220 and 50-410
License Nos: DPR-63 and NPF-69
Enclosure:      Inspection Report 05000220/2013003 and 05000410/2013003
                  w/Attachment: Supplementary Information
cc w/encl:      Distribution via ListServ


SUBJECT: NINE MILE POINT NUCLEAR STATION - NRC INTEGRATED INSPECTION REPORT 05000220/2013003 AND 05000410/2013003
Dear Mr. Costanzo:


   
  ML13225A471
On June 30, 2013, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at
                                                Non-Sensitive                              Publicly Available
your Nine Mile Point Nuclear Station (NMPNS) Units 1 and 2. The enclosed inspection report documents the inspection results, which were
        SUNSI Review
discussed on July 25, 2013, with you and other members of your staff.
                                                Sensitive                                  Non-Publicly Available
OFFICE    klm      RI/DRP                RI/DRP                  RI/DRP
NAME              KKolaczyk/DLS for    ARosebrook/DLS for      DSchroeder/DLS
DATE              08/13/13              08/13/13                08/13/13
                                               
                                        1
              U.S. NUCLEAR REGULATORY COMMISSION
                                  REGION I
Docket Nos:  50-220 and 50-410
License Nos: DPR-63 and NPF-69
Report No:  05000220/2013003 and 05000410/2013003
Licensee:    Constellation Energy Nuclear Group, LLC (CENG)
Facility:    Nine Mile Point Nuclear Station, Units 1 and 2
Location:    Oswego, NY
Dates:      April 1, 2013 through June 30, 2013
Inspectors:  K. Kolaczyk, Senior Resident Inspector
            E. Miller, Resident Inspector
            B. Dionne, Health Physicist
            B. Haagensen, Resident Inspector
            P. Kaufman, Senior Reactor Inspector
            J. Krafty, Resident Inspector
            J. Laughlin, Emergency Preparedness Inspector
            J. Lilliendahl, Reactor Inspector
            A. Rosebrook, Senior Project Engineer
            B. Scrabeck, Project Engineer
Approved by: Daniel L. Schroeder, Chief
            Reactor Projects Branch 1
            Division of Reactor Projects
                                                            Enclosure


   
                                                                2
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your licenseThe inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.  
                                              TABLE OF CONTENTS
SUMMARY.................................................................................................................................... 3
1. REACTOR SAFETY.............................................................................................................. 7
    1R01  Adverse Weather Protection ................................................................................... 7
    1R04  Equipment Alignment .............................................................................................. 8
    1R05  Fire Protection ......................................................................................................... 9
    1R07  Heat Sink Performance ........................................................................................... 9
    1R08  Inservice Inspection Activities ............................................................................... 10
    1R11  Licensed Operator Requalification Program & Licensed Operator Performance .. 12
    1R12  Maintenance Effectiveness ................................................................................... 13
    1R13  Maintenance Risk Assessments and Emergent Work Control .............................. 13
    1R15  Operability Determinations and Functionality Assessments.................................. 14
    1R18  Plant Modifications ................................................................................................ 15
    1R19  Post-Maintenance Testing ..................................................................................... 15
    1R20  Refueling and Other Outage Activities .................................................................. 16
    1R22  Surveillance Testing .............................................................................................. 17
    1EP4  Emergency Action Level and Emergency Plan Changes ...................................... 20
    1EP6  Drill Evaluation ...................................................................................................... 20
2.  RADIATION SAFETY.......................................................................................................... 21
    2RS1  Radiological Hazard Assessment and Exposure Controls .................................... 21
    2RS2  Occupational ALARA Planning and Controls ........................................................ 24
    2RS3  In-Plant Airborne Radioactivity Control and Mitigation .......................................... 26
    2RS4  Occupational Dose Assessment ........................................................................... 27
    2RS7  Radiological Environmental Monitoring Program .................................................. 30
4OTHER ACTIVITIES ........................................................................................................... 33
    4OA1  Performance Indicator Verification ........................................................................ 33
    4OA2  Problem Identification and Resolution ................................................................... 33
    4OA3  Follow-Up of Events and Notices of Enforcement Discretion ................................ 42
    4OA6  Meetings, Including Exit ........................................................................................ 50
ATTACHMENT: SUPPLEMENTARY INFORMATION .............................................................. 50
SUPPLEMENTARY INFORMATION ........................................................................................ A-1
KEY POINTS OF CONTACT .................................................................................................... A-1
LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED ..................................... A-2
LIST OF DOCUMENTS REVIEWED ........................................................................................ A-3
LIST OF ACRONYMS............................................................................................................. A-19
                                                                                                                            Enclosure


                                                    3
This report documents one self-revealing apparent violation concerning the improper restoration
                                                SUMMARY
of a direct current electrical bus which resulted in a loss of all shutdown cooling. The safety  
IR 05000220/2013003, 05000410/2013003; 04/01/2013 - 06/30/2013; Nine Mile Point Nuclear
significance of the violation is still under review pending the outcome of a Phase III risk analysis by NRC Senior Reactor Analysts. However, the violation does not represent an immediate safety concern because Constellation has conducted a prompt human performance event review, entered the issue into their corrective action program (CAP), and conducted a root  
Station (NMPNS) Units 1 and 2; Surveillance Testing, Problem Identification and Resolution,
cause analysis. Additionally, corrective actions including a review of all emergency, off-normal,  
Follow-Up of Events and Notices of Enforcement Discretion.
and normal system operating procedures are in progress. This violation with the supporting circumstances and details is documented in this inspection report.
This report covered a 3-month period of inspection by resident inspectors and announced
inspections performed by regional inspectors. One apparent violation was identified. The
This report documents two NRC-identified findings and two self-revealing findings of very low
safety significance of this violation is still under review pending the outcome of a Phase III risk
safety significance (Green). These findings were determined to involve violations of NRC
analysis by NRC Senior Reactor Analysts. Additionally, two NRC-identified findings and two
requirements.  However, because of the very low safety significance, and because they are
self-revealing findings of very low safety significance (Green) were identified, all of which were
entered into your CAP, the NRC is treating these findings as non-cited violations (NCVs) consistent with Section 2.3.2 of the NRC Enforcement Policy.  If you contest any NCVs in this report, you should provide a response within 30 days of the date of this inspection report with
non-cited violations (NCVs). The significance of most findings is indicated by their color (i.e.,
the basis of your denial, to the U.S. Nuclear Regulatory Commission, ATTN:  Document Control
greater than Green, or Green, White, Yellow, Red) and determined using Inspection Manual
Desk, Washington D.C. 20555-0001; with copies to the Regional Administrator, Region I; the
Chapter (IMC) 0609, Significance Determination Process (SDP), dated June 2, 2011. Cross-
Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the NRC Resident Inspector at NMPNS. In addition, if you disagree with the  
cutting aspects are determined using IMC 0310, Components Within the Cross-Cutting Areas,
C. Costanzo
dated October 28, 2011. All violations of NRC requirements are dispositioned in accordance
2cross-cutting aspect assigned to any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region I, and the NRC Resident Inspector at NMPNS. 
with the NRCs Enforcement Policy, dated January 28, 2013. The NRCs program for
overseeing the safe operation of commercial nuclear power reactors is described in NUREG-
1649, Reactor Oversight Process, Revision 4.
Cornerstone: Initiating Events
  TBD. A self-revealing apparent violation of Technical Specification (TS) 6.4.1, Procedures,
    was identified at Unit 1 because CENG failed to properly recover from a loss of a vital direct
    current (DC) bus in accordance with station off-normal procedures resulting in an unplanned
    loss of all shutdown cooling (SDC) when time to boil was less than 2 hours. Specifically,
    during the restoration from the loss of battery bus 12, operators failed to identify a SDC trip
    signal before attempting restoration of the DC bus, which ultimately lead to a SDC pump trip
    (i.e. loss of decay heat removal from the reactor). Corrective actions included conducting a
    prompt human performance event review, entering the issue into their corrective action
    program (CAP), and conducting a root cause analysis. Planned corrective actions include a
    review of all emergency, off-normal, and normal system operating procedures.
    The inspectors determined that CENGs failure to properly restore battery bus 12 in
    accordance with N1-SOP-47A.1, Loss of DC, Revision 00101, and N1-OP-47A, 125 VDC
    Power System, Revision 02500, was a performance deficiency that was reasonably within
    CENGs ability to foresee and correct and should have been prevented. The performance
    deficiency was determined to be more than minor because the inspectors determined it
    affected the configuration control aspect of the Initiating Events cornerstone and adversely
    affected the associated cornerstone objective to limit the likelihood of events that upset plant
    stability and challenge critical safety functions during shutdown as well as power operations.
    The significance of the finding is designated as To Be Determined (TBD) until a Phase 3
    analysis can be completed by the NRCs Senior Reactor Analysts. The inspectors
    determined this finding has a cross-cutting aspect in the area of Human Performance,
    Resources, because CENG did not ensure that personnel, equipment, procedures, and
    other resources were available and adequate to assure nuclear safety - complete, accurate
                                                                                          Enclosure


                                                  4
In accordance with Title 10 of the Code of Federal Regulations
  and up-to-date design documentation, procedures, work packages, and correct labeling of
2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly
  components. Specifically, CENG procedures N1-SOP-47A.1 and N1-OP-47A did not
Available Records component of the NRC's Agencywide Documents Access Management System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).  
  contain adequate guidance to ensure recovery from a loss of a DC bus would not result in
Sincerely,  
  an unexpected plant transient [H.2(c)]. (Section 4OA3)
Cornerstone: Mitigating Systems
/RA/ 
  Green. A self-revealing NCV of TS 5.4.1, Procedures, was identified at Unit 2 when a
Daniel L. Schroeder, Chief Reactor Projects Branch 1
  CENG instrumentation and control (I&C) technician did not properly implement procedure
Division of Reactor Projects
  N2-ISP-LDS-Q010, Reactor Building General Area Temperature Instrument Channel
  Functional Test, Revision 00102. As a result, a residual heat removal (RHR)/reactor core
Docket Nos: 50-220 and 50-410
  isolation cooling (RCIC) isolation bypass switch was inadvertently left in the NORMAL
License Nos: DPR-63 and NPF-69
  position during surveillance testing resulting in an unplanned RCIC isolation. CENG entered
Enclosure:  Inspection Report 05000220/2013003 and 05000410/2013003
  this issue into their CAP as CR-2013-002461. Other corrective actions included performing
              w/Attachment:  Supplementary Information
  a human performance stand down that reinforced use of human performance tools and the
  need to identify and mark critical steps during pre-job briefs, retraining the I&C technicians
  involved in the event on proper use of human performance error prevention techniques, and
  improving bypass switch verification steps for procedure N2-ISP-LDS-Q010 and other
  similar lead detection system surveillances procedures.
  This finding is more than minor because it is associated with the human performance
  attribute of the Mitigating Systems cornerstone and affected the cornerstone objective to
  ensure the availability, reliability, and capability of systems that respond to initiating events
  to prevent undesirable consequences (i.e., core damage). Specifically, the inadvertent
  isolation rendered the RCIC system inoperable and unable to perform its function for
  approximately 6 hours. Additionally, this finding is similar to example 4.b of IMC 0612,
  Appendix E, Examples of Minor issues, and is more than minor due to the procedural error
  leading to a plant transient, i.e. an unplanned RCIC isolation. This finding was evaluated in
  accordance with IMC 0609.04, Initial Characterization of Findings, and Exhibit 2 of IMC
  0609, Appendix A, The Significance Determination Process for Findings At-Power, issued
  June 19, 2012. Unit 2 is a boiling-water reactor (BWR)-5, and as a result, RCIC is treated
  as having a separate high-pressure injection safety function. A detailed analysis was
  conducted using SAPHIRE version 8.0.8.0 and Unit 2 SPAR model 8.17. Using an
  exposure period of 6 hours and conservatively assuming no recovery of the failed
  equipment, this finding had a change in core damage frequency of low E-8. The dominant
  accident sequence was a grid-related loss of offsite power with a failure of Division III power
  and the failure to recover offsite power and the emergency diesel generators (EDGs) in 30
  minutes. Since the change in core damage frequency was less than 1E-7, contributions
  from large early release and external event did not need to be considered. Therefore, this
  finding was of very low safety significance (Green). This finding has a cross-cutting aspect
  in the area of Human Performance, Work Practices, because the I&C technicians did not
  effectively employ self-checking and place-keeping when implementing the test procedure
  which directly contributed to the resulting procedural error [H.4(a)]. (Section 1R22)
  Green. The inspectors identified an NCV at Unit 2 of Title 10 of the Code of Federal
  Regulations (10 CFR) Part 50, Appendix B, Criterion V, Instructions, Procedures, and
  Drawings, because CENG did not assure that the replacement of cells in battery 2C were
  prescribed and performed by appropriate procedures which resulted in degraded accuracy
                                                                                            Enclosure


                                                    5
cc w/encl:   Distribution via ListServ
  of test results and potential degradation of safety-related battery cells. In response to this
    
  issue, CENG generated CR-2013-005235 and initiated actions to evaluate replacing the
  new cells.
  This finding is more than minor because it was associated with the equipment performance
  attribute of the Mitigating Systems cornerstone and affected the cornerstone objective to
    
  ensure the availability, reliability, and capability of systems that respond to initiating events
 
  to prevent undesirable consequences. In accordance with IMC 0609.04, Initial
  Characterization of Findings, and Exhibit 2 of IMC 0609, Appendix A, The Significance
  Determination Process for Findings At-Power, issued June 19, 2012, the inspectors
  determined this finding is of very low safety significance (Green) because the performance
  deficiency was not a design or qualification deficiency, did not involve an actual loss of
  safety function, did not represent actual loss of a safety function of a single train for greater
  than its TS allowed outage time, and did not screen as potentially risk-significant due to a
  seismic, flooding, or severe weather initiating event. This finding has a cross-cutting aspect
  in the area of Human Performance, Decision-Making component, because CENG did not
  use conservative assumptions in decision making. Specifically, CENG did not monitor the
  cells in storage, question the adequacy of the discharged cells, charge the cells prior to
  installation, or fully evaluate the implications of the test and recharge results [H.1(b)].
  (Section 4OA2)
  Green. The inspectors identified an NCV at Unit 2 of 10 CFR Part 50, Appendix B,
  Criterion III, Design Control, because CENG did not verify the adequacy of the design with
  respect to battery 2C. Specifically, by failing to size the battery to the most limiting time
  period, the sizing calculation significantly overstated the available design margin. CENGs
  corrective actions included generating condition report CR-2013-005117 and evaluating the
  condition for operability.
  This finding is more than minor because it was associated with the design control attribute of
  the Mitigating Systems cornerstone and affected the cornerstone objective to ensure the
  availability, reliability, and capability of systems that respond to initiating events to prevent
  undesirable consequences. In accordance with IMC 0609.04, Initial Characterization of
  Findings, and Exhibit 2 of IMC 0609, Appendix A, The Significance Determination Process
  for Findings At-Power, issued June 19, 2012, the inspectors determined this finding is of
  very low safety significance (Green) because the performance deficiency was not a design
  or qualification deficiency, did not involve an actual loss of safety function, did not represent
  actual loss of a safety function of a single train for greater than its TS allowed outage time,
  and did not screen as potentially risk-significant due to a seismic, flooding, or severe
  weather initiating event. The inspectors did not assign a cross-cutting aspect because the
  finding was not indicative of current performance. (Section 4OA2)
Cornerstone: Barrier Integrity
   Green. A self-revealing NCV of TS 3.3.3, Leakage Rate, was identified for CENGs failure
  from December 3 to December 13, 2012, to maintain containment leakage less than
  1.5 percent by weight of the containment air per day and less than 0.6 percent by weight of
  the containment air per day for all penetrations and all primary containment isolation valves
   subject to 10 CFR Part 50, Appendix J, Types B and C tests, when pressurized to
                                                                                            Enclosure


                                              6
35 pound per square inch gauge when reactor coolant system (RCS) temperature is above
215°F and primary containment integrity is required. CENG entered this issue into their
CAP as CR-2012-011247. Corrective actions included cleaning iron oxide from the primary
containment vent and purge valve and replacing the resilient seals.
This finding is more than minor because it is associated with the structure, system,
component (SSC), and barrier performance attribute of the Barrier Integrity cornerstone and
affected the cornerstone objective to provide reasonable assurance that physical design
barriers (fuel cladding, reactor coolant system, and containment) protect the public from
radionuclide releases caused by accidents or events. Specifically, containment leakage
exceeded the leakage limits outlined in the Unit 1 TS 3.3.3 from December 3 to December
13, 2012. This finding was evaluated in accordance with IMC 0609.04, Initial
Characterization of Findings, and Table 6.2, Phase 2 Risk Significance-Type B Findings at
Full Power, of IMC 0609, Appendix H, Containment Integrity Significance Determination
Process, issued May 6, 2004. The inspectors determined this finding was of very low
safety significance (Green) because the leakage was less than 100 percent of containment
volume per day for the duration of the leak. This finding has a cross-cutting aspect in the
area of Problem Identification and Resolution, CAP, because CENG failed to take
appropriate corrective action to address safety issues and adverse trends in a timely
manner commensurate with their safety significance. Specifically, following identification of
the adverse trend regarding the frequency of nitrogen addition to the drywell, CENG did not
assess in a timely manner the significance of the leakage and the impact on primary plant
containment [P.1(d)]. (Section 4OA3)
                                                                                    Enclosure


ML13225A471  SUNSI Review
                                                  7
  Non-Sensitive  Sensitive
                                        REPORT DETAILS
Publicly Available Non-Publicly Available OFFICE    klm RI/DRP RI/DRP RI/DRP  NAME KKolaczyk/DLS for ARosebrook/DLS for DSchroeder/DLS  DATE 08/13/13 08/13/13 08/13/13 
Summary of Plant Status
Unit 1 began the inspection period at 100 percent power. On April 14, 2013, Unit 1 reduced
Enclosure
power to 32 percent to conduct emergency condenser testing and to down power for refueling
1 U.S. NUCLEAR REGULATORY COMMISSION
outage (N1R22). On April 15, Unit 1 was removed from the grid to commence N1R22. Unit 1
REGION I  Docket Nos: 50-220 and 50-410
returned to service and synchronized to the grid on May 15. On June 21, Unit 1 down powered
    
to 83 percent to perform a rod pattern adjustment, turbine stop valve replacement, and a reactor
License Nos:  DPR-63 and NPF-69
recirculation pump swap. Unit 1 returned to rated power on June 22 and remained at or near
full power for the remainder of the inspection period.
Unit 2 began the inspection period at 100 percent power. On May 28, Unit 2 down powered to
65 percent to investigate diverging feedwater flows between two operating feedwater pumps.
Following identification of a degraded automatic feedwater regulating valve and removal of the
B feedwater pump from service, Unit 2 returned to 100 percent on May 31, and remained at or
near full power for the remainder of the inspection period.
1.     REACTOR SAFETY
        Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
1R01 Adverse Weather Protection (71111.01 - 2 samples)
.1      Readiness for Seasonal Extreme Weather Conditions
   a.    Inspection Scope
        The inspectors performed a review of CENGs readiness for the onset of seasonal high
        temperatures. The review focused on Unit 1 fire protection and diesel fire pump,
        technical support center ventilation, control room and reactor building (RB) air
        conditioning systems, and Unit 2 service water and heating, ventilation, and air
        conditioning systems. The inspectors reviewed the Updated Final Safety Analysis
        Report (UFSAR), TSs, and the CAP to determine what temperatures or other seasonal
        weather could challenge these systems and to ensure CENG personnel had adequately
        prepared for these challenges. The inspectors reviewed station procedures including
        CENGs seasonal weather readiness procedure and applicable operating procedures.
        The inspectors performed walkdowns of the selected systems to ensure station
        personnel identified issues that could challenge the operability of the systems during hot
        weather conditions. Documents reviewed for each section of this inspection report are
        listed in the Attachment.
  b.    Findings
        No findings were identified.
                                                                                        Enclosure


                                                8
Report No:  05000220/2013003 and 05000410/2013003
.2  Summer Readiness of Offsite and Alternate Alternating Current (AC) Power Systems
   a. Inspection Scope
    The inspectors performed a review of plant features and procedures for the operation
Licensee:  Constellation Energy Nuclear Group, LLC (CENG)
    and continued availability of the offsite and alternate AC power system to evaluate
 
    readiness of the systems prior to seasonal high grid loading. The inspectors reviewed
    changes to CENGs procedures affecting these areas and the communications protocols
Facility:  Nine Mile Point Nuclear Station, Units 1 and 2
    between the transmission system operator and CENG implemented since the previous
    sample in 2012. This review focused on changes to the established program and
    material condition of the offsite and alternate AC power equipment. The inspectors
Location:  Oswego, NY
    assessed whether CENG established and implemented appropriate procedures and
  Dates:  April 1, 2013 through June 30, 2013
    protocols to monitor and maintain availability and reliability of both the offsite ac power
 
    system and the onsite alternate AC power system. The inspectors evaluated the material
    condition of the associated equipment by interviewing the season readiness coordinator,
    reviewing condition reports and open work orders and walking down portions of the
Inspectors:  K. Kolaczyk, Senior Resident Inspector    E. Miller, Resident Inspector    B. Dionne, Health Physicist
    offsite and AC power systems including the 345 kilovolt (kV) and 115 kV switchyards.
  B. Haagensen, Resident Inspector
   b. Findings
  P. Kaufman, Senior Reactor Inspector
    No findings were identified.
  J. Krafty, Resident Inspector
  J. Laughlin, Emergency Preparedness Inspector    J. Lilliendahl, Reactor Inspector    A. Rosebrook, Senior Project Engineer
  B. Scrabeck, Project Engineer
 
Approved by:  Daniel L. Schroeder, Chief Reactor Projects Branch 1
 
Division of Reactor Projects
 
Enclosure
2  TABLE OF CONTENTS SUMMARY ...............................................................................................................................
..... 3 1. REACTOR SAFETY.............................................................................................................. 7
1R01 Adverse Weather Protection ................................................................................... 7
1R04 Equipment Alignment .............................................................................................. 8
1R05 Fire Protection ......................................................................................................... 9
1R07 Heat Sink Performance ........................................................................................... 9
1R08 Inservice Inspection Activities ............................................................................... 10
1R11 Licensed Operator Requalification Program & Licensed Operator Performance .. 12
1R12 Maintenance Effectiveness ................................................................................... 13
1R13 Maintenance Risk Assessments and Emergent Work Control .............................. 13
1R15 Operability Determinations and Functionality Assessments
.................................. 14
1R18 Plant Modifications ................................................................................................ 15
1R19 Post-Maintenance Testing ..................................................................................... 15
1R20 Refueling and Other Outage Activities .................................................................. 16
1R22 Surveillance Testing .............................................................................................. 17
1EP4 Emergency Action Level and Emergency Plan Changes ...................................... 20
1EP6 Drill Evaluation ...................................................................................................... 20
2. RADIATION SAFETY.......................................................................................................... 21
2RS1 Radiological Hazard Assessment and Exposure Controls .................................... 21
2RS2 Occupational ALARA Planning and Controls ........................................................ 24
2RS3 In-Plant Airborne Radioactivity Control and Mitigation .......................................... 26
2RS4 Occupational Dose Assessment ........................................................................... 27
2RS7 Radiological Environmental Monitoring Program .................................................. 30
4. OTHER ACTIVITIES ........................................................................................................... 33
4OA1 Performance Indicator Verification ........................................................................ 33
4OA2 Problem Identification and Resolution ................................................................... 33
4OA3 Follow-Up of Events and Notices of Enforcement Discretion ................................ 42
4OA6 Meetings, Including Exit ........................................................................................ 50
ATTACHMENT:  SUPPLEMENTARY INFORMATION .............................................................. 50
SUPPLEMENTARY INFORMATION ........................................................................................ A-1
KEY POINTS OF CONTACT .................................................................................................... A-1
LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED ..................................... A-2
LIST OF DOCUMENTS REVIEWED ........................................................................................ A-3
LIST OF ACRONYMS
............................................................................................................. A-19
Enclosure
3 SUMMARY  IR 05000220/2013003, 05000410/2013003; 04/01/2013 - 06/30/2013; Nine Mile Point Nuclear Station (NMPNS) Units 1 and 2; Surveillance Testing, Problem Identification and Resolution,
Follow-Up of Events and Notices of Enforcement Discretion.
 
This report covered a 3-month period of inspection by resident inspectors and announced
inspections performed by regional inspectors.  One apparent violation was identified.  The safety significance of this violation is still under review pending the outcome of a Phase III risk analysis by NRC Senior Reactor Analysts.  Additionally, two NRC-identified findings and two self-revealing findings of very low safety significance (Green) were identified, all of which were 
non-cited violations (NCVs).  The significance of most findings is indicated by their color (i.e.,
greater than Green, or Green, White, Yellow, Red) and determined using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process (SDP)," dated June 2, 2011.  Cross-cutting aspects are determined using IMC 0310, "Components Within the Cross-Cutting Areas,"
 
dated October 28, 2011.  All violations of NRC requirements are dispositioned in accordance with the NRC's Enforcement Policy, dated January 28, 2013.  The NRC's program for
overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4.
Cornerstone: Initiating Events
  TBD.  A self-revealing apparent violation of Technical Specification (TS) 6.4.1, "Procedures," was identified at Unit 1 because CENG failed to properly recover from a loss of a vital direct current (DC) bus in accordance with station off-normal procedures resulting in an unplanned
loss of all shutdown cooling (SDC) when time to boil was less than 2 hours.  Specifically, during the restoration from the loss of battery bus 12, operators failed to identify a SDC trip signal before attempting restoration of the DC bus, which ultimately lead to a SDC pump trip
(i.e. loss of decay heat removal from the reactor).  Corrective actions included conducting a
 
prompt human performance event review, entering the issue into their corrective action program (CAP), and conducting a root cause analysis.  Planned corrective actions include a review of all emergency, off-normal, and normal system operating procedures.
   The inspectors determined that CENG's failure to properly restore battery bus 12 in
accordance with N1-SOP-47A.1, "Loss of DC," Revision 00101, and N1-OP-47A, "125 VDC
Power System," Revision 02500, was a performance deficiency that was reasonably within
CENG's ability to foresee and correct and should have been prevented.  The performance deficiency was determined to be more than minor because the inspectors determined it affected the configuration control aspect of the Initiating Events cornerstone and adversely affected the associated cornerstone objective to limit the likelihood of events that upset plant
stability and challenge critical safety functions during shutdown as well as power operations. 
The significance of the finding is designated as To Be Determined (TBD) until a Phase 3 analysis can be completed by the NRC's Senior Reactor Analysts.  The inspectors determined this finding has a cross-cutting aspect in the area of Human Performance,
Resources, because CENG did not ensure that personnel, equipment, procedures, and
other resources were available and adequate to assure nuclear safety - complete, accurate 
 
 
Enclosure
and up-to-date design documentation, procedures, work packages, and correct labeling of components.  Specifically, CENG procedures N1-SOP-47A.1 and N1-OP-47A did not  contain adequate guidance to ensure recovery from a loss of a DC bus would not result in
an unexpected plant transient [H.2(c)]. (Section 4OA3)
  Cornerstone:  Mitigating Systems
  Green.  A self-revealing NCV of TS 5.4.1, "Procedures," was identified at Unit 2 when a CENG instrumentation and control (I&C) technician did not properly implement procedure N2-ISP-LDS-Q010, "Reactor Building General Area Temperature Instrument Channel Functional Test," Revision 00102.  As a result, a residual heat removal (RHR)/reactor core
isolation cooling (RCIC) isolation bypass switch was inadvertently left in the NORMAL position during surveillance testing resulting in an unplanned RCIC isolation.  CENG entered
this issue into their CAP as CR-2013-002461.  Other corrective actions included performing a human performance stand down that reinforced use of human performance tools and the need to identify and mark critical steps during pre-job briefs, retraining the I&C technicians
involved in the event on proper use of human performance error prevention techniques, and
improving bypass switch verification steps for procedure N2-ISP-LDS-Q010 and other
similar lead detection system surveillances procedures.
  This finding is more than minor because it is associated with the human performance attribute of the Mitigating Systems cornerstone and affected the cornerstone objective to
ensure the availability, reliability, and capability of systems that respond to initiating events
to prevent undesirable consequences (i.e., core damage).  Specifically, the inadvertent isolation rendered the RCIC system inoperable and unable to perform its function for approximately 6 hours.  Additionally, this finding is similar to example 4.b of IMC 0612, Appendix E, "Examples of Minor issues," and is more than minor due to the procedural error
leading to a plant transient, i.e. an unplanned RCIC isolation.  This finding was evaluated in
accordance with IMC 0609.04, "Initial Characterization of Findings," and Exhibit 2 of IMC
0609, Appendix A, "The Significance Determination Process for Findings At-Power," issued June 19, 2012.  Unit 2 is a boiling-water reactor (BWR)-5, and as a result, RCIC is treated as having a separate high-pressure injection safety function.  A detailed analysis was
conducted using SAPHIRE version 8.0.8.0 and Unit 2 SPAR model 8.17.  Using an
exposure period of 6 hours and conservatively assuming no recovery of the failed
equipment, this finding had a change in core damage frequency of low E-8.  The dominant
accident sequence was a grid-related loss of offsite power with a failure of Division III power and the failure to recover offsite power and the emergency diesel generators (EDGs) in 30 minutes.  Since the change in core damage frequency was less than 1E-7, contributions
from large early release and external event did not need to be considered.  Therefore, this
finding was of very low safety significance (Green).  This finding has a cross-cutting aspect in the area of Human Performance, Work Practices, because the I&C technicians did not effectively employ self-checking and place-
keeping when implementing the test procedure which directly contributed to the resulting procedural error [H.4(a)].  (Section 1R22)
 
  Green.  The inspectors identified an NCV at Unit 2 of Title 10 of the
Code of Federal
Regulations (10 CFR) Part 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," because CENG did not assure that the replacement of cells in battery 2C were
prescribed and performed by appropriate procedures which resulted in degraded accuracy 
 
Enclosure
of test results and potential degradation of safety-related battery cells.  In response to this  issue, CENG generated CR-2013-005235 and initiated actions to evaluate replacing the new cells.
 
This finding is more than minor because it was associated with the equipment performance
attribute of the Mitigating Systems cornerstone and affected the cornerstone objective to 
ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.  In accordance with IMC 0609.04, "Initial Characterization of Findings," and Exhibit 2 of IMC 0609, Appendix A, "The Significance
Determination Process for Findings At-Power," issued June 19, 2012, the inspectors
determined this finding is of very low safety significance (Green) because the performance deficiency was not a design or qualification deficiency, did not involve an actual loss of safety function, did not represent actual loss of a safety function of a single train for greater than its TS allowed outage time, and did not screen as potentially risk-significant due to a
seismic, flooding, or severe weather initiating event.  This finding has a cross-cutting aspect
in the area of Human Performance, Decision-Making component, because CENG did not
use conservative assumptions in decision making.  Specifically, CENG did not monitor the cells in storage, question the adequacy of the discharged cells, charge the cells prior to installation, or fully evaluate the implications of the test and recharge results [H.1(b)]. 
(Section 4OA2)
 
  Green.  The inspectors identified an NCV at Unit 2 of 10 CFR Part 50, Appendix B, Criterion III, "Design Control," because CENG did not verify the adequacy of the design with respect to battery 2C.  Specifically, by failing to size the battery to the most limiting time period, the sizing calculation significantly overstated the available design margin.  CENG's corrective actions included generating condition report CR-2013-005117 and evaluating the condition for operability.
 
This finding is more than minor because it was associated with the design control attribute of
the Mitigating Systems cornerstone and affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.  In accordance with IMC 0609.04, "Initial Characterization of
Findings," and Exhibit 2 of IMC 0609, Appendix A, "The Significance Determination Process
for Findings At-Power," issued June 19, 2012, the inspectors determined this finding is of
very low safety significance (Green) because the performance deficiency was not a design
or qualification deficiency, did not involve an actual loss of safety function, did not represent actual loss of a safety function of a single train for greater than its TS allowed outage time, and did not screen as potentially risk-significant due to a seismic, flooding, or severe
weather initiating event.  The inspectors did not assign a cross-cutting aspect because the
finding was not indicative of current performance.  (Section 4OA2)
 
Cornerstone:  Barrier Integrity
  Green.  A self-revealing NCV of TS 3.3.3, "Leakage Rate," was identified for CENG's failure from December 3 to December 13, 2012, to maintain containment leakage less than  1.5 percent by weight of the containment air per day and less than 0.6 percent by weight of
the containment air per day for all penetrations
and all primary containment isolation valves subject to 10 CFR Part 50, Appendix J, Types 'B' and 'C' tests, when pressurized to 
 
Enclosure
35 pound per square inch gauge when reactor coolant system (RCS) temperature is above 215°F and primary containment integrity is required.  CENG entered this issue into their CAP as CR-2012-011247.  Corrective actions included cleaning iron oxide from the primary containment vent and purge valve and replacing the resilient seals.
 
This finding is more than minor because it is associated with the structure, system,
component (SSC), and barrier performance attribute of the Barrier Integrity cornerstone and affected the cornerstone objective to provide reasonable assurance that physical design barriers (fuel cladding, reactor coolant system, and containment) protect the public from
radionuclide releases caused by accidents or
events.  Specifically, containment leakage exceeded the leakage limits outlined in the Unit 1 TS 3.3.3 from December 3 to December
13, 2012.  This finding was evaluated in accordance with IMC 0609.04, "Initial Characterization of Findings," and Table 6.2, "Phase 2 Risk Significance-Type B Findings at Full Power," of IMC 0609, Appendix H, "Containment Integrity Significance Determination
Process," issued May 6, 2004.  The inspectors determined this finding was of very low
safety significance (Green) because the leakage was less than 100 percent of containment
volume per day for the duration of the leak.  This finding has a cross-cutting aspect in the area of Problem Identification and Resolution, CAP, because CENG failed to take appropriate corrective action to address safety issues and adverse trends in a timely
manner commensurate with their safety significance.  Specifically, following identification of the adverse trend regarding the frequency of nitrogen addition to the drywell, CENG did not
assess in a timely manner the significance of the leakage and the impact on primary plant
 
containment [P.1(d)].  (Section 4OA3)
   
Enclosure
7REPORT DETAILS
  Summary of Plant Status
 
Unit 1 began the inspection period at 100 percent power.  On April 14, 2013, Unit 1 reduced
power to 32 percent to conduct emergency condenser testing and to down power for refueling
outage (N1R22).  On April 15, Unit 1 was removed from the grid to commence N1R22.  Unit 1
returned to service and synchronized to the grid on May 15.  On June 21, Unit 1 down powered to 83 percent to perform a rod pattern adjustment, turbine stop valve replacement, and a reactor recirculation pump swap.  Unit 1 returned to rated power on June 22 and remained at or near
full power for the remainder of the inspection period.
 
Unit 2 began the inspection period at 100 percent power. On May 28, Unit 2 down powered to 65 percent to investigate diverging feedwater flows between two operating feedwater pumps.  Following identification of a degraded automatic feedwater regulating valve and removal of the
'B' feedwater pump from service, Unit 2 returned to 100 percent on May 31, and remained at or
near full power for the remainder of the inspection period.
 
1. REACTOR SAFETY
  Cornerstones:  Initiating Events, Mitigating Systems, and Barrier Integrity
1R01 Adverse Weather Protection (71111.01 - 2
samples)  .1 Readiness for Seasonal Extreme Weather Conditions
 
  a.  Inspection Scope
  The inspectors performed a review of CENG's readiness for the onset of seasonal high temperatures.  The review focused on Unit 1 fire protection and diesel fire pump, technical support center ventilation, control room and reactor building (RB) air
conditioning systems, and Unit 2 service water and heating, ventilation, and air
conditioning systems.  The inspectors reviewed the Updated Final Safety Analysis
Report (UFSAR), TSs, and the CAP
to determine what temperatures or other seasonal weather could challenge these systems and to ensure CENG personnel had adequately prepared for these challenges.  The inspectors reviewed station procedures including CENG's seasonal weather readiness procedure and applicable operating procedures. 
The inspectors performed walkdowns of the selected systems to ensure station
personnel identified issues that could challenge the operability of the systems during hot weather conditions.  Documents reviewed for each section of this inspection report are listed in the Attachment.
  b.  Findings
  No findings were identified.
 
 
8  Enclosure .2 Summer Readiness of Offsite and Alternate Alternating Current (AC) Power Systems
 
   a. Inspection Scope
  The inspectors performed a review of plant features and procedures for the operation  
and continued availability of the offsite and alternate AC power system to evaluate  
readiness of the systems prior to seasonal high grid loading. The inspectors reviewed  
changes to CENG's procedures affecting these areas and the communications protocols  
between the transmission system operator and CENG implemented since the previous sample in 2012. This review focused on changes to the established program and material condition of the offsite and alternate AC power equipment. The inspectors  
assessed whether CENG established and implemented appropriate procedures and  
protocols to monitor and maintain availability and reliability of both the offsite ac power  
system and the onsite alternate AC power system. The inspectors evaluated the material condition of the associated equipment by interviewing the season readiness coordinator, reviewing condition reports and open work orders and walking down portions of the  
offsite and AC power systems including the 345  
kilovolt (kV) and 115 kV switchyards.
   b. Findings
  No findings were identified.  
1R04 Equipment Alignment
1R04 Equipment Alignment
 
    Partial System Walkdown (71111.04Q - 5 samples)
Partial System Walkdown (71111.04Q - 5 samples)  
  a. Inspection Scope
  a. Inspection Scope
    The inspectors performed partial walkdowns of the following systems:
 
        Unit 1, Spent fuel pool (SFP) cooling system during the conduct of refueling
The inspectors performed partial walkdowns of the following systems:  
        maintenance related activities on April 15, 2013
        Unit 1, Core sprays 112 and 122 following the completion of surveillance activities on
        April 21, 2013
        Unit 1, Isolation condenser loop 12 following the completion of maintenance activities
        on May 15, 2013
        Unit 1, Diesel and electric fire pumps while the maintenance fire pump was operating
        with a degraded discharge relief valve on May 22, 2013
        Unit 1, Control room emergency ventilation system following the completion of
        maintenance activities on May 30, 2013
    The inspectors selected these systems based on their risk-significance relative to the
    reactor safety cornerstones at the time they were inspected. The inspectors reviewed
    applicable operating procedures, system diagrams, the UFSAR, TSs, work orders,
    condition reports, and the impact of ongoing work activities on redundant trains of
    equipment in order to identify conditions that could have impacted system performance
    of their intended safety functions. The inspectors also performed field walkdowns of
    accessible portions of the systems to verify system components and support equipment
    were aligned correctly and were operable. The inspectors examined the material
    condition of the components and observed operating parameters of equipment to verify
                                                                                        Enclosure


  Unit 1, Spent fuel pool (SFP) cooling system during the conduct of refueling maintenance related activities on April 15, 2013  Unit 1, Core sprays 112 and 122 following the completion of surveillance activities on April 21, 2013  Unit 1, Isolation condenser loop 12 following the completion of maintenance activities on May 15, 2013  Unit 1, Diesel and electric fire pumps while the maintenance fire pump was operating with a degraded discharge relief valve on May 22, 2013  Unit 1, Control room emergency ventilation system following the completion of  maintenance activities on May 30, 2013
                                                9
The inspectors selected these systems based on their risk-significance relative to the
    that there were no deficiencies. The inspectors also reviewed whether CENG staff had
reactor safety cornerstones at the time they were inspected.  The inspectors reviewed
    properly identified equipment issues and entered them into the CAP for resolution with
applicable operating procedures, system diagrams, the UFSAR, TSs, work orders,
    the appropriate significance characterization.
condition reports, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have impacted system performance of their intended safety functions.  The inspectors also performed field walkdowns of
b.  Findings
accessible portions of the systems to verify system components and support equipment were aligned correctly and were operable.  The inspectors examined the material
    No findings were identified.
condition of the components and observed operat
ing parameters of equipment to verify 
9  Enclosure that there were no deficiencies. The inspectors also reviewed whether CENG staff had properly identified equipment issues and entered them into the CAP for resolution with  
the appropriate significance characterization.  
  b.  Findings
  No findings were identified.  
1R05 Fire Protection
1R05 Fire Protection
  Resident Inspector Quarterly Walkdowns (71111.05Q - 6 samples)  
    Resident Inspector Quarterly Walkdowns (71111.05Q - 6 samples)
   
  a. Inspection Scope
  a. Inspection Scope
    The inspectors conducted tours of the areas listed below to assess the material
  The inspectors conducted tours of the areas listed below to assess the material condition and operational status of fire protection features.  The inspectors verified that  
    condition and operational status of fire protection features. The inspectors verified that
    CENG controlled combustible materials and ignition sources in accordance with
    administrative procedures. The inspectors verified that fire protection and suppression
    equipment was available for use as specified in the area pre-fire plan, and passive fire
    barriers were maintained in good material condition. The inspectors also verified that
    station personnel implemented compensatory measures for out of service, degraded, or
    inoperable fire protection equipment, as applicable, in accordance with procedures.
        Unit 1, Drywell (FA3/R1) on April 16, 2013
        Unit 1, RB elevation 340 feet (FA1/R6A and FA2/R6B) on April 19, 2013
        Unit 1, RB elevation 198 feet southwest (FA2/R1B) on April 21, 2013
        Unit 1, RB elevation 237 feet east (FA1/R1A) on April 21, 2013
        Unit 1, RB elevation 237 feet west (FA2/R1B) on April 21, 2013
        Unit 1, Power board 12 (FA-17A) on April 26, 2013
  b.  Findings
    No findings were identified.
1R07 Heat Sink Performance (71111.07 - 2 samples)
a.  Inspection Scope
    The inspectors reviewed the samples listed below to determine their readiness and
    availability to perform their safety functions. The inspectors reviewed the design basis
    for the components and verified CENGs commitments to NRC Generic Letter 89-13.
    The inspectors discussed the results of the most recent inspection with engineering staff
    and reviewed pictures of the as-found and as-left conditions. The inspectors verified that
    CENG initiated appropriate corrective actions for identified deficiencies.
        Unit 1, Emergency diesel generator (EDG) 103 raw water heat exchanger on
          May 3, 2013
        Unit 2, 2HVY*UC2A service water pump bay A unit cooler on May 7, 2013
                                                                                      Enclosure


CENG controlled combustible materials and ignition sources in accordance with administrative procedures. The inspectors verified that fire protection and suppression
                                              10
equipment was available for use as specified in the area pre-fire plan, and passive fire barriers were maintained in good material condition. The inspectors also verified that
1R08 Inservice Inspection Activities (71111.08 - 1 sample)
station personnel implemented compensatory measures for out of service, degraded, or inoperable fire protection equipment, as applicable, in accordance with procedures.  
a.  Inspection Scope
    From April 15 to 18, 2013, the inspectors conducted a review of CENGs implementation
    of inservice inspection (ISI) program activities for monitoring degradation of the RCS
    boundary and risk-significant piping system boundaries for Unit 1 during the N1R22.
    The sample selection was based on the inspection procedure objectives and risk priority
    of those components and systems where degradation would result in a significant
    increase in risk of core damage. The inspectors observed in-process nondestructive
    examinations (NDEs), reviewed documentation, and interviewed CENG personnel to
    verify that the NDE activities performed were conducted in accordance with the
    requirements of the American Society of Mechanical Engineers (ASME) Boiler and
    Pressure Vessel Code, Section XI, 2004 Edition.
    NDE Activities and Welding Activities
    The inspectors performed direct observations of NDE activities in process and reviewed
    records of NDEs listed below:
    ASME Code Required Examinations
        Remote visual examination (VT-3) of reactor vessel nozzle N16-1-N3A and manual
          ultrasonic testing (UT) examination of three 12-inch diameter emergency condenser
          supply piping welds.
        Data records of manual UT phased array examination of five 28-inch diameter
          reactor vessel nozzle-to-vessel dissimilar metal safe end-to-nozzle welds (32-WD-
          042, N2A; 32-WD-082, N2B; 32-WD-122, N2C; 32-WD-164, N2D; 32-WD-208, N2E),
          manual UT of four 12-inch diameter emergency condenser supply piping welds, dye
          penetrant testing and UT of branch connection-decontamination port welds on the
          recirculation system suction piping, and UT thickness readings of various diameter
          RB closed loop cooling system piping located at elevation 225 foot in the drywell.
    The inspectors reviewed certifications of the NDE technician, process, and equipment in
    identifying the condition or degradation of risk-significant SSCs and evaluated the
    activities for compliance with the requirements of Unit 1s risk informed ISI program,
    ASME Boiler and Pressure Vessel Code, Section XI, and 10 CFR 50.55a.
    Augmented or Industry Imitative Examinations
    Based on industry operating experience, the inspectors reviewed NDE data records of
    the recirculation system suction piping decontamination port branch connection welds to
    verify that the activities were performed in accordance with applicable examination
    procedures and industry guidance.
    Modification/Repair/Replacement Consisting of Welding Activities
    The inspectors reviewed the following welding activities to verify specifications and
    control of the welding processes, weld procedures, welder qualifications, and NDE
    examinations were in accordance with ASME code requirements.
                                                                                      Enclosure


  Unit 1, Drywell (FA3/R1) on April 16, 2013  Unit 1, RB elevation 340 feet (FA1/R6A and FA2/R6B) on April 19, 2013  Unit 1, RB elevation 198 feet southwest (FA2/R1B) on April 21, 2013  Unit 1, RB elevation 237 feet east (FA1/R1A) on April 21, 2013  Unit 1, RB elevation 237 feet west (FA2/R1B) on April 21, 2013  Unit 1, Power board 12 (FA-17A) on April 26, 2013
                                            11
   b. Findings
  The repair and replacement of reactor water cleanup (RWCU) dissimilar metal pipe weld
   No findings were identified.  
  33-WD-046 was reviewed. The inspectors reviewed the associated flaw evaluation,
  NDE data records, and repair/replacement WO package.
  During manual phased array UT of a 6-inch diameter schedule 80 stainless steel pipe to
  carbon steel RWCU pipe dissimilar metal weld, a 4.25-inch long circumferential flaw
  indication was detected in the heat-affected zone of the stainless steel side of the weld.
  The indication did not meet ASME Code, Section XI 2004, IWB-3514-2 acceptance
  criteria so a flaw evaluation was required. The flaw evaluation concluded that sufficient
  structural margin was demonstrated for the as-found flaw indication.
  However, a review of construction radiographs by CENG indicated that there had been
  two previous weld repairs directly adjacent to this indication. CENG determined that the
  residual stresses of the weld were likely to be high due to the prior weld repairs and the
  crack growth rate would be high enough to possibly propagate the flaw beyond the
  ASME code limit of through-thickness. Based on this information, CENG replaced the
  weld and adjacent pipe by installing a new spool piece.
  The inspectors verified the welding activities and applicable NDE techniques were
  performed in accordance with ASME Code requirements.
  Re-examination of an Indication Previously Accepted for Service After Analysis
  There were no samples available for review during this inspection that involved
  examinations with recordable indications that have been accepted for continued service
  from the previous Unit 1 outage through the current outage.
  Drywell Visual Examination
  The inspectors examined the condition of Unit 1 drywell liner surface at various elevation
  levels inside the drywell. During the inspection, surface corrosion was noted on the
  drywell liner and on several systems including the RB closed-cooling water system.
  CENG was monitoring the condition of the liner and RB closed-cooling water system to
  ensure the corrosion was not impacting system or component operability.
  Identification and Resolution of Problems
  The inspectors reviewed a sample of condition reports which involved ISI-related
  activities to confirm that non-conformances were being properly identified, reported, and
   resolved.
b. Findings
   No findings were identified.
                                                                                    Enclosure


                                                12
1R07 Heat Sink Performance (71111.07 - 2 samples)  
1R11 Licensed Operator Requalification Program and Licensed Operator Performance
  a. Inspection Scope
    (71111.11Q - 4 samples)
   The inspectors reviewed the samples listed below to determine their readiness and
.1   Quarterly Review of Licensed Operator Requalification Testing and Training (2 samples)
availability to perform their safety functions.  The inspectors reviewed the design basis
for the components and verified CENG's commitments to NRC Generic Letter 89-13. 
The inspectors discussed the results of the most recent inspection with engineering staff  and reviewed pictures of the as-found and as-left conditions.  The inspectors verified that CENG initiated appropriate corrective actions for identified deficiencies. 
 
  Unit 1, Emergency diesel generator (EDG) 103 raw water heat exchanger on  May 3, 2013  Unit 2, 2HVY*UC2A service water pump bay 'A' unit cooler on May 7, 2013
 
10  Enclosure 1R08 Inservice Inspection Activities (71111.08 - 1 sample)  
   a. Inspection Scope
   a. Inspection Scope
  From April 15 to 18, 2013, the inspectors conducted a review of CENG's implementation
    The inspectors observed:
of inservice inspection (ISI) program activities for monitoring degradation of the RCS
        Unit 1, Licensed operator simulator training which included a loss of condenser
boundary and risk-significant piping system boundaries for Unit 1 during the N1R22. 
        vacuum, a stuck open electro-matic relief valve (ERV), and an anticipated transient
The sample selection was based on the inspection procedure objectives and risk priority
        without scram on April 2, 2013
of those components and systems where degradation would result in a significant increase in risk of core damage.  The inspectors observed in-process nondestructive examinations (NDEs), reviewed documentat
        Unit 2, Licensed operator performance during a simulator training scenario that
ion, and interviewed CENG personnel to verify that the NDE activities performed were conducted in accordance with the
        included high temperatures on the main transformer, degraded service water, and a
requirements of the American Society of Mechanical Engineers (ASME) Boiler and
        loss of the offsite electrical grid on May 23, 2013
Pressure Vessel Code, Section XI, 2004 Edition. 
    The inspectors evaluated operator performance during the simulated event and verified
NDE Activities and Welding Activities
    completion of risk-significant operator actions, including the use of abnormal and
 
    emergency operating procedures. The inspectors assessed the clarity and effectiveness
The inspectors performed direct observations of NDE activities in process and reviewed
    of communications, implementation of actions in response to alarms and degrading plant
records of NDEs listed below:
    conditions, and the oversight and direction provided by the control room supervisor. The
ASME Code Required Examinations
    inspectors verified the accuracy and timeliness of the emergency classifications made by
  Remote visual examination (VT-3) of reactor vessel nozzle N16-1-N3A and manual ultrasonic testing (UT) examination of
    the shift manager and the TS action statements entered by the shift technical advisor.
three 12-inch diameter emergency condenser supply piping welds.  Data records of manual UT phased array examination of five 28-inch diameter reactor vessel nozzle-to-vessel dissimilar metal safe end-to-nozzle welds (32-WD-042, N2A; 32-WD-082, N2B; 32-WD-122, N2C; 32-WD-164, N2D; 32-WD-208, N2E),
    Additionally, the inspectors assessed the ability of the crew and training staff to identify
manual UT of four 12-inch diameter emergency condenser supply piping welds, dye penetrant testing and UT of branch connection-decontamination port welds on the recirculation system suction piping, and UT thickness readings of various diameter
    and document crew performance problems.
RB closed loop cooling system piping located at elevation 225 foot in the drywell.
The inspectors reviewed certifications of the NDE technician, process, and equipment in identifying the condition or degradation of risk-significant SSCs and evaluated the activities for compliance with the requirements of Unit 1's risk informed ISI program,
ASME Boiler and Pressure Vessel Code, Section XI, and 10 CFR 50.55a.
 
Augmented or Industry Imitative Examinations
  Based on industry operating experience, the inspectors reviewed NDE data records of the recirculation system suction piping decontamination port branch connection welds to
verify that the activities were performed in accordance with applicable examination
procedures and industry guidance.
 
Modification/Repair/Replacement Consisting of Welding Activities
 
The inspectors reviewed the following welding activities to verify specifications and control of the welding processes, weld procedures, welder qualifications, and NDE
examinations were in accordance with ASME code requirements.
 
11  Enclosure The repair and replacement of reactor water cleanup (RWCU) dissimilar metal pipe weld 33-WD-046 was reviewed.  The inspectors reviewed the associated flaw evaluation,
NDE data records, and repair/replacement WO package.
During manual phased array UT of a 6-inch diameter schedule 80 stainless steel pipe to
carbon steel RWCU pipe dissimilar metal weld, a 4.25-inch long circumferential flaw
indication was detected in the heat-affected zone of the stainless steel side of the weld. 
The indication did not meet ASME Code, Section XI 2004, IWB-3514-2 acceptance
criteria so a flaw evaluation was required.  The flaw evaluation concluded that sufficient structural margin was demonstrated for the as-found flaw indication.
However, a review of construction radiographs by CENG indicated that there had been
two previous weld repairs directly adjacent to this indication.  CENG determined that the residual stresses of the weld were likely to be high due to the prior weld repairs and the crack growth rate would be high enough to possibly propagate the flaw beyond the ASME code limit of through-thickness.  Based on this information, CENG replaced the
weld and adjacent pipe by installing a new spool piece.
 
The inspectors verified the welding activities and applicable NDE techniques were
performed in accordance with ASME Code requirements.
Re-examination of an Indication Previously Accepted for Service After Analysis
 
There were no samples available for review during this inspection that involved
examinations with recordable indications that have been accepted for continued service from the previous Unit 1 outage through the current outage.
Drywell Visual Examination
 
The inspectors examined the condition of Unit 1 drywell liner surface at various elevation levels inside the drywell.  During the inspection, surface corrosion was noted on the drywell liner and on several systems including the RB closed-cooling water system. 
CENG was monitoring the condition of the liner and RB closed-cooling water system to ensure the corrosion was not impacting system or component operability.
Identification and Resolution of Problems
 
The inspectors reviewed a sample of condition reports which involved ISI-related
activities to confirm that non-conformances were being properly identified, reported, and
 
resolved.
  b. Findings
 
No findings were identified.
 
 
 
12  Enclosure 1R11 Licensed Operator Requalification Program and Licensed Operator Performance
(71111.11Q - 4 samples)
.1 Quarterly Review of Licensed Operator Requalification Testing and Training (2 samples)
  a. Inspection Scope
  The inspectors observed:  
 
  Unit 1, Licensed operator simulator training which included a loss of condenser vacuum, a stuck open electro-matic relief valve (ERV), and an anticipated transient without scram on April 2, 2013 Unit 2, Licensed operator performance during a simulator training scenario that included high temperatures on the main transformer, degraded service water, and a loss of the offsite electrical grid on May 23, 2013  
The inspectors evaluated operator performance during the simulated event and verified  
completion of risk-significant operator actions, including the use of abnormal and emergency operating procedures. The inspectors assessed the clarity and effectiveness of communications, implementation of actions in response to alarms and degrading plant  
conditions, and the oversight and direction provided by the control room supervisor. The inspectors verified the accuracy and timeliness of the emergency classifications made by  
the shift manager and the TS action statements entered by the shift technical advisor. Additionally, the inspectors assessed the ability of the crew and training staff to identify  
and document crew performance problems.  
   b. Findings
   b. Findings
 
    No findings were identified.
No findings were identified.  
.2   Quarterly Review of Licensed Operator Performance in the Main Control Room
.2 Quarterly Review of Licensed Operator Performance in the Main Control Room
    (2 samples)
  (2 samples)  
   a. Inspection Scope
   a. Inspection Scope
  The inspectors observed:  
    The inspectors observed:
        Unit 2, Control room operations during a period of increased site activity due to a
        failure of an on-site power loop that supplied electrical power to several non-
        essential buildings within the protected area as well as several plant information
        technology systems on April 9, 2013
        Unit 1, Control room operations during a plant shutdown to commence planned
        refueling outage N1R22 on April 14, 2013
    The inspectors reviewed CNG-OP-1.01-1000, Conduct of Operations, Revision 00900,
    and verified that procedure use, crew communications, and coordination of plant
    activities among work groups similarly met established expectations and standards.
    Additionally, the inspectors observed test performance to verify that procedure use, crew
    communications, and coordination of activities between work groups similarly met
    established expectations and standards.
                                                                                        Enclosure


  Unit 2, Control room operations during a period of increased site activity due to a failure of an on-site power loop that supplied electrical power to several non-essential buildings within the protected area as well as several plant information
                                              13
technology systems on April 9, 2013 Unit 1, Control room operations during a plant shutdown to commence planned refueling outage N1R22 on April 14, 2013  
b.  Findings
  The inspectors reviewed CNG-OP-1.01-1000, "Conduct of Operations," Revision 00900,  
    No findings were identified.
and verified that procedure use, crew communications, and coordination of plant
1R12 Maintenance Effectiveness (71111.12Q - 4 samples)
a.  Inspection Scope
    The inspectors reviewed the samples listed below to assess the effectiveness of
    maintenance activities on SSC performance and reliability. The inspectors reviewed
    system health reports, CAP documents, maintenance work orders, and maintenance
    rule basis documents to ensure that CENG was identifying and properly evaluating
    performance problems within the scope of the maintenance rule. For each sample
    selected, the inspectors verified that the SSC was properly scoped into the maintenance
    rule in accordance with 10 CFR 50.65 and verified that the (a)(2) performance criteria
    established by CENG staff was reasonable. As applicable, for SSCs classified as (a)(1),
    the inspectors assessed the adequacy of goals and corrective actions to return these
    SSCs to (a)(2). Additionally, the inspectors ensured that CENG staff was identifying and
    addressing common cause failures that occurred within and across maintenance rule
    system boundaries.
        Unit 1, Neutron monitoring on May 14, 2013
        Unit 2, High-pressure core spray (HPCS) on May 14, 2013
        Unit 1, Service water on May 16, 2013
        Unit 1, Containment spray on May 17, 2013
  b.  Findings
    No findings were identified.
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13 - 8 samples)
a.  Inspection Scope
    The inspectors reviewed station evaluation and management of plant risk for the
    maintenance and emergent work activities listed below to verify that CENG performed
    the appropriate risk assessments prior to removing equipment from service. The
    inspectors selected these activities based on potential risk significance relative to the
    reactor safety cornerstones. As applicable for each activity, the inspectors verified that
    CENG personnel performed risk assessments as required by 10 CFR 50.65(a)(4) and
    that the assessments were accurate and complete. When CENG performed emergent
    work, the inspectors verified that operations personnel promptly assessed and managed
    plant risk. The inspectors reviewed the scope of maintenance work and discussed the
    results of the assessment with the stations probabilistic risk analyst to verify plant
    conditions were consistent with the risk assessment. The inspectors also reviewed the
    TS requirements and inspected portions of redundant safety systems, when applicable,
    to verify risk analysis assumptions were valid and applicable requirements were met.
                                                                                        Enclosure


activities among work groups similarly met established expectations and standards.  Additionally, the inspectors observed test performance to verify that procedure use, crew
                                              14
communications, and coordination of activities between work groups similarly met established expectations and standards. 
        Unit 2, Unplanned elevated risk condition that resulted from an inadvertent isolation
13  Enclosure
        of the RCIC system on April 2, 2013
  b. Findings
        Unit 2, Loss of maintenance supply power to 2VBB*UPS3B on April 5, 2013
  No findings were identified.  
        Unit 1, Power boards 102 and 16 following electrical realignment on May 1, 2013
        Unit 1, Planned maintenance on pressure safety valve 201.970, emergency
1R12 Maintenance Effectiveness (71111.12Q - 4 samples)  
        condenser vent isolation IV-05-03, and emergency condenser 112 HX HTX-60-44 on
   
        May 2, 2013
  a. Inspection Scope
        Unit 2, Planned maintenance on the Division I control room air conditioning system
  The inspectors reviewed the samples listed below to assess the effectiveness of maintenance activities on SSC performance and reliability.  The inspectors reviewed
        on May 13, 2013
system health reports, CAP documents, maintenance work orders, and maintenance
        Unit 1, Unplanned maintenance on the turbine bypass valve control system on
rule basis documents
        May 14, 2013
to ensure that CENG
        Unit 1, Planned maintenance on the 102 EDG raw water pump on May 23, 2013
was identifying and properly evaluating performance problems within the scope of the maintenance rule. For each sample selected, the inspectors verified that the SSC was properly scoped into the maintenance rule in accordance with 10 CFR 50.65 and verified that the (a)(2) performance criteria  
        Unit 2, Unplanned maintenance on the 2SWP*P1B service water pump on June 11,
established by CENG staff was reasonable.  As applicable, for SSCs classified as (a)(1),
        2013
the inspectors assessed the adequacy of goals and corrective actions to return these
  b. Findings
SSCs to (a)(2).  Additionally, the inspectors ensured that CENG
    No findings were identified.
staff was identifying and addressing common cause failures that occurred within and across maintenance rule system boundaries.  
1R15 Operability Determinations and Functionality Assessments (71111.15 - 9 samples)
  a. Inspection Scope
    The inspectors reviewed operability determinations for the following degraded or non-
    conforming conditions:
        Unit 1, Acceptance criteria associated with N1-ST-C5, secondary containment, and
        RB emergency ventilation system operability testing on April 13, 2013
        Unit 1, Emergency service water 11 pump (72-04) trip during surveillance testing on
        April 17, 2013
        Unit 1, Damaged containment spray nozzle deflectors on May 3, 2013
        Unit 1, Source range monitors due to under-vessel work on May 3, 2013
        Unit 1, Steam leakage from vent valve 05-11 on May 19, 2013
        Unit 2, RCIC high-energy line break barrier door on May 20, 2013
        Unit 1, Core spray topping pump 122 bearing cooling water flow on June 11, 2013
        Unit 2, Elevated drywell floor drain leakage on June 11, 2013
        Unit 1, Elevated drywell floor drain leakage on June 25, 2013
    The inspectors selected these issues based on the risk significance of the associated
    components and systems. The inspectors evaluated the technical adequacy of the
    operability determinations to assess whether TS operability was properly justified and
    the subject component or system remained available such that no unrecognized
    increase in risk occurred. The inspectors compared the operability and design criteria in
    the appropriate sections of the TSs and UFSAR to CENGs evaluations to determine
    whether the components or systems were operable. Where compensatory measures
    were required to maintain operability, the inspectors determined whether the measures
    in place would function as intended and were properly controlled by CENG. The
    inspectors determined, where appropriate, compliance with bounding limitations
    associated with the evaluations.
                                                                                    Enclosure


  Unit 1, Neutron monitoring on May 14, 2013  Unit 2, High-pressure core spray (HPCS) on May 14, 2013  Unit 1, Service water on May 16, 2013  Unit 1, Containment spray on May 17, 2013
                                                15
  b. Findings
 
No findings were identified.
 
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13 - 8 samples)
  a. Inspection Scope
  The inspectors reviewed station evaluation and management of plant risk for the
 
maintenance and emergent work activities listed below to verify that CENG performed the appropriate risk assessments prior to removing equipment from service.  The inspectors selected these activities based on potential risk significance relative to the reactor safety cornerstones.  As applicable for each activity, the inspectors verified that
CENG personnel performed risk assessments as required by 10 CFR 50.65(a)(4) and
that the assessments were accurate and complete.  When CENG performed emergent
work, the inspectors verified that operations personnel promptly assessed and managed plant risk.  The inspectors reviewed the scope of maintenance work and discussed the results of the assessment with the station's probabilistic risk analyst to verify plant
conditions were consistent with the risk assessment.  The inspectors also reviewed the
TS requirements and inspected portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met.
 
 
14  Enclosure  Unit 2, Unplanned elevated risk condition that resulted from an inadvertent isolation of the RCIC system on April 2, 2013  Unit 2, Loss of maintenance supply power to 2VBB*UPS3B on April 5, 2013  Unit 1, Power boards 102 and 16 following electrical realignment on May 1, 2013  Unit 1, Planned maintenance on pressure safety valve 201.970, emergency condenser vent isolation IV-05-03, and emergency condenser 112 HX HTX-60-44 on May 2, 2013
  Unit 2, Planned maintenance on the Division I control room air conditioning system on May 13, 2013  Unit 1, Unplanned maintenance on the turbine bypass valve control system on May 14, 2013  Unit 1, Planned maintenance on the 102 EDG raw water pump on May 23, 2013  Unit 2, Unplanned maintenance on the 2SWP*P1B service water pump on June 11, 2013 
   b. Findings
   b. Findings
  No findings were identified.  
    No findings were identified.
 
1R18 Plant Modifications (71111.18 - 3 samples)
1R15 Operability Determinations and Functionality Assessments (71111.15 - 9 samples)
.1   Temporary Modifications (1 sample)
  a. Inspection Scope
 
The inspectors reviewed operability determinations for the following degraded or non-conforming conditions:
  Unit 1, Acceptance criteria associated with N1-ST-C5, secondary containment, and RB emergency ventilation system operability testing on April 13, 2013  Unit 1, Emergency service water 11 pump (72-04) trip during surveillance testing on April 17, 2013  Unit 1, Damaged containment spray nozzle deflectors on May 3, 2013  Unit 1, Source range monitors due to under-vessel work on May 3, 2013  Unit 1, Steam leakage from vent valve 05-11 on May 19, 2013  Unit 2, RCIC high-energy line break barrier door on May 20, 2013  Unit 1, Core spray topping pump 122 bearing cooling water flow on June 11, 2013  Unit 2, Elevated drywell floor drain leakage on June 11, 2013  Unit 1, Elevated drywell floor drain leakage on June 25, 2013 
The inspectors selected these issues based on the risk significance of the associated
components and systems.  The inspectors evaluated the technical adequacy of the
operability determinations to assess whether TS operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred.  The inspectors compared the operability and design criteria in
the appropriate sections of the TSs and UFSAR to CENG's evaluations to determine
 
whether the components or systems were
operable.  Where compensatory measures were required to maintain operability, the inspectors determined whether the measures
in place would function as intended and were properly controlled by CENG.  The inspectors determined, where appropriate, compliance with bounding limitations associated with the evaluations.
 
15  Enclosure  b. Findings
 
No findings were identified.
1R18 Plant Modifications (71111.18 - 3 samples)  
.1 Temporary Modifications (1 sample)  
   a. Inspection Scope
   a. Inspection Scope
  The inspectors reviewed a temporary change to ventilation damper 2HVP*AOD5A which  
    The inspectors reviewed a temporary change to ventilation damper 2HVP*AOD5A which
supplies outside air to the Division III diesel generator room. The inspectors reviewed  
    supplies outside air to the Division III diesel generator room. The inspectors reviewed
10 CFR 50.59 documentation and conducted a field walkdown of the modification to  
    10 CFR 50.59 documentation and conducted a field walkdown of the modification to
verify that the temporary modification did not degrade the design bases, licensing bases, and performance capability of the affected systems.  
    verify that the temporary modification did not degrade the design bases, licensing bases,
    and performance capability of the affected systems.
   b. Findings
   b. Findings
  No findings were identified.  
    No findings were identified.
.2 Permanent Modifications (2 samples)  
.2   Permanent Modifications (2 samples)
   a. Inspection Scope
   a. Inspection Scope
  The inspectors evaluated the following modifications:  
    The inspectors evaluated the following modifications:
  Engineering Change Package (ECP) 12-00616 - Installation of a damper for Unit 1  
        Engineering Change Package (ECP) 12-00616 - Installation of a damper for Unit 1
downstream of BV-210-25 ECP 13-000167 - Installation of replacement pump for Unit 1 service water radiation  
        downstream of BV-210-25
monitor The inspectors verified that the design bases, licensing bases, and performance capability of the affected system was not degraded by the modifications. In addition, the inspectors reviewed modification documents associated with the upgrade and design  
        ECP 13-000167 - Installation of replacement pump for Unit 1 service water radiation
change including the post-installation test procedure, the 10 CFR 50.59 screening form,  
        monitor
and the operational impact assessment form.
    The inspectors verified that the design bases, licensing bases, and performance
    capability of the affected system was not degraded by the modifications. In addition, the
    inspectors reviewed modification documents associated with the upgrade and design
    change including the post-installation test procedure, the 10 CFR 50.59 screening form,
    and the operational impact assessment form.
   b. Findings
   b. Findings
  No findings were identified.  
    No findings were identified.
 
1R19 Post-Maintenance Testing (71111.19 - 5 samples)
1R19 Post-Maintenance Testing (71111.19 - 5 samples)  
  a. Inspection Scope
  The inspectors reviewed the post-maintenance tests for the maintenance activities listed
below to verify that procedures and test activities ensured system operability and
functional capability.  The inspectors reviewed the test procedure to verify that the procedure adequately tested the safety functions that may have been affected by the maintenance activity, that the acceptance criteria in the procedure was consistent with 
16  Enclosure the information in the applicable licensing basis and/or design basis documents, and that the procedure had been properly reviewed and approved.  The inspectors also
witnessed the test or reviewed test data to verify that the test results adequately demonstrated restoration of the affected safety functions.
 
  Unit 1, Control room ventilation/smoke purge system test following installation of fire damper BV-21-036 on April 3, 2013  Unit 1, Power board 102 following National Fire Protection Act 805 modification on April 28, 2013  Unit 1, Isolation valve IV-39-10R following control circuit stop relay replacement on May 9, 2013  Unit 1, Replacement of excess flow check valve CKV-32-138 on May 10, 2013  Unit 1, IV-29-07R diagnostic testing following body-to-bonnet seal replacement on May 23, 2013
  b. Findings
  No findings were identified.
1R20 Refueling and Other Outage Activities (71111.20 - 1 sample)
   a. Inspection Scope
   a. Inspection Scope
  The inspectors reviewed the station's work schedule and outage risk plan for the Unit 1 maintenance and refueling outage (N1R22) which was conducted April 14 through May 15, 2013.  The inspectors reviewed CENG's development and implementation of outage
    The inspectors reviewed the post-maintenance tests for the maintenance activities listed
plans and schedules to verify that risk, industry experience, previous site-specific problems, and defense-in-depth were considered.  During the outage, the inspectors
    below to verify that procedures and test activities ensured system operability and
observed portions of the shutdown and cooldown processes and monitored controls associated with the following outage activities:
    functional capability. The inspectors reviewed the test procedure to verify that the
  Configuration management, including maintenance of defense-in-depth, commensurate with the outage plan for the key safety functions and compliance with the applicable TSs when taking equipment out of service  Implementation of clearance activities and confirmation that tags were properly hung and that equipment was appropriately configured to safely support the associated
    procedure adequately tested the safety functions that may have been affected by the
work or testing  Installation and configuration of reactor coolant pressure, level, and temperature instruments to provide accurate indication and instrument error accounting  Status and configuration of electrical systems and switchyard activities to ensure that  
    maintenance activity, that the acceptance criteria in the procedure was consistent with
TSs were met  Monitoring of decay heat removal operations  Impact of outage work on the ability of the operators to operate the SFP cooling system  Reactor water inventory controls, including flow paths, configurations, alternative means for inventory additions, and controls to prevent inventory loss  Activities that could affect reactivity  Maintenance of secondary containment as required by TSs  Refueling activities   Fatigue management 
                                                                                      Enclosure
17  Enclosure  Tracking of startup prerequisites, walkdown of the drywell (primary containment) to verify that debris had not been left which could block the emergency core cooling system suction strainers, and startup and ascension to full power  Identification and resolution of problems related to refueling activities
  b. Findings
  No findings were identified.
1R22 Surveillance Testing (71111.22 - 8 samples)
  a. Inspection Scope
  The inspectors observed performance of surveillance tests and/or reviewed test data of
selected risk-significant SSCs to assess whether test results satisfied TSs, the UFSAR,
and CENG procedure requirements. The inspectors verified that test acceptance criteria
were clear, tests demonstrated operational readiness and were consistent with design
documentation, test instrumentation had current calibrations and the range and accuracy for the application, tests were performed as written, and applicable test prerequisites were satisfied.  Upon test completion, the inspectors considered whether the test results
supported that equipment was capable of performing the required safety functions.  The inspectors reviewed the following surveillance tests:
  N1-ST-Q3, Unit 1, High-Pressure Coolant Injection Pump and Check Valve Operability Test for Train 12 on April 1, 2013  N1-ST-C5, Unit 1, Secondary Containment and Reactor Building Emergency Ventilation System Operability Test for Loop 11 on April 8, 2013  N1-ISP-LRT-TYC, Unit 1, Local Leak Rate Test for Valves IV-201-09 and IV-201-10 on April 9, 2013
  N2-ISP-LDS-Q010, Unit 2, Reactor Building General Area Temperature Instrument Channel Functional Test on April 18, 2013  Unit 2, RCS Leakage Determination Surveillance and Calculations on April 24, 2013  N2-CSP-GEN-D100, Unit 2, Reactor Water/Auxiliary Water Chemistry Surveillance on April 24, 2013  N1-TSP-201-001, Unit 1, Integrated Leak Rate Test of Primary Containment Type 'A'
Test on May 8, 2013  N1-ST-Q15, Unit 1, Condensate Transfer System Operability Test on May 30, 2013
  b. Findings
  Introduction.  A self-revealing Green NCV of TS 5.4.1, "Procedures," was identified at Unit 2 when a CENG I&C technician did not properly implement procedure N2-ISP-LDS-
Q010, "Reactor Building General Area Temperature Instrument Channel Functional Test," Revision 00102.  As a result, a RHR/RCIC isolation bypass switch was inadvertently left in the NORMAL position during surveillance testing resulting in an unplanned RCIC isolation.
Description.  The RCIC system is designed to provide adequate makeup water to the reactor pressure vessel (RPV) automatica
lly or manually following an RPV isolation accompanied by a loss of coolant flow from the feedwater system.  In the event the 
18  Enclosure steam piping to the RCIC pump system leaks, temperature sensors in the RCIC pump room will close isolation valves in the RCIC system stopping the leak.  CENG
surveillance procedure N2-ISP-LDS-Q010 is a TS surveillance test that verifies that the group 5 (RHR) and group 10 (RCIC) isolation trip signals will close the respective
system isolation valves if a high-temperature condition occurs.  The procedure tests this function by simulating a high temperature condition and verifying correct system response.  Actual valve movement during testing is prevented by control room operators blocking the test signal. 
On April 2, 2013, an unplanned RCIC isolation occurred when I&C technicians did not properly implement procedure N2-ISP-LDS-Q010 to block the test signal.  Specifically,
step 7.2.1 required I&C technicians to request control room operators to place channel
bypass switch E31A-S4B RHR/RCIC ISOLATION BYPASS in BYPASS and to verify the  
circuit was bypassed by observing annunciator and plant computer alarms prior to lifting thermocouple leads in the field.  This was not accomplished which resulted in the isolation of the RCIC system. 
Prior to the event, a pre-job brief was conducted by CENG I&C technicians performing the work which focused on the roles and responsibilities of personnel including the lifting of thermocouple leads safely and error free.  Placing the RHR/RCIC isolation bypass switch in BYPASS was not identified as a critical step, and no critical steps were
annotated in the work document as required by CNG-PR-1.01-1009, "Procedure and
 
Work Order Use and Adherence Requirements," Revision 00701.  However, the
 
requirement for operations personnel to
place the isolation switch in BYPASS was discussed during the procedure review with the control room supervisor who assigned a control room operator to perform the task when requested by I&C technicians.  Section 3.12 of CNG-PR-1.01-1009 defines place-keeping as physically marking steps to
prevent the omission or duplication of the steps to maintain an accounting of steps in
progress, steps completed, steps not applicable, and steps not yet performed.  It lists
among high-risk practices to be avoided by signing or checking off a step as completed before it is completed.  After commencing surveillance procedure N2-ISP-LDS-Q010, technicians used improper self-checking and place-keeping by checking and initialing as
complete step 7.2.1 to request operators to place the RHR/RCIC isolation bypass switch
in BYPASS and to verify annunciator and computer alarm points were in alarm without
that step having been performed.  Consequently, when thermocouple leads were lifted in
the following step, a false high-temperature signal was generated resulting in the closing of RCIC steam supply isolation valves 2ICS*MOV121, 2ICS*MOV128, 2ICS*MOV170, and an unplanned isolation of RCIC.  The surveillance test was immediately stopped, the
required TS action statements were entered for the RCIC system, and the system was
restored to an operable status after approximately 6 hours.  The isolation signal was also
sent to the RHR system for SDC supply and return valves and for reactor head spray isolation valve which were already closed
at power.  There was no impact on operability of low-pressure coolant injection or containment spray functions of RHR. 
A CENG investigation concluded human error as the primary cause for the inadvertent
isolation of the RCIC system.  A contributing cause was the failure to implement
adequate corrective actions following a similar RCIC isolation event in 2007.  Immediate corrective actions for this event included a human performance stand down that reinforced use of human performance tools and the need to identify and mark critical
steps during pre-job briefs, retraining the I&C technicians involved in the event on proper
 
use of human performance error prevention techniques, and improving bypass switch 
19  Enclosure verification steps for procedure N2-ISP-LDS-Q010 and other similar leak detection system surveillance procedures.  CENG entered this issue in their CAP as CR-2013-
 
002461.  Analysis.  The inspectors determined that CENG's failure to correctly implement surveillance test procedure N2-ISP-LDS-Q010 was a performance deficiency that was
within CENG's ability to foresee and correct and should have been prevented.  This
finding is more than minor because it is associated with the human performance attribute
of the Mitigating Systems cornerstone and affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage).  Specifically, the inadvertent
isolation rendered the RCIC system inoperable and unable to perform its function for
approximately 6 hours.  Additionally, this finding is similar to Example 4.b. of IMC 0612, Appendix E, "Examples of Minor Issues," and is more than minor due to the procedural error leading to a plant transient, i.e. an unplanned RCIC isolation. 
In accordance with IMC 0609.04, "Initial Characterization of Findings," and Exhibit 2 of
IMC 0609, Appendix A, "The Significance Determination Process for Findings At-Power,"
issued June 19, 2012, this finding represents a loss of safety function.  Unit 2 is a BWR-5, and as a result, RCIC is treated as having a separate high- pressure injection safety function.  A detailed analysis was conducted using SAPHIRE Version 8.0.8.0 and Unit 2 SPAR Model 8.17.  Using an exposure period of 6 hours and conservatively
assuming no recovery of the failed equipment, this finding had a change in core damage
frequency of low E-8.  The dominant accident sequence was a grid- related loss of off-
site power with a failure of Division III power and the failure to recover off-site power and the EDGs in 30 minutes.  Since the change in core damage frequency was less than
1E-7, contributions from large early release and external event did not need to be considered.  Therefore, this finding was determined to be of very low safety significance
(Green). 
This finding had a cross-cutting aspect in the area of Human Performance, Work Practices, because the I&C technicians did not effectively employ self-checking and
 
place-keeping when implementing N2-ISP-LDS-Q010 which directly contributed to the resulting procedural error [H.4(a)].
Enforcement.  TS 5.4.1, "Procedures," requires written procedures to be established, implemented, and maintained covering the applicable procedures recommended in Regulatory Guide (RG) 1.33, "Quality Assurance Program Requirements (Operation),"
Appendix A, Revision 2, dated February 1978.  Section 8.b(2)(b) of RG 1.33 requires, in
part, specific procedures for surveillance tests on containment isolation.  CENG surveillance test procedure N2-ISP-LDS-Q010, "Reactor Building General Area Temperature Instrument Channel Functional Test," directed that the RHR/RCIC ISOLATION BYPASS switch be placed in BYPASS to prevent an inadvertent
containment isolation while lifting thermocouple leads.  Contrary to above, on April 2,
2013, technicians lifted thermocouple leads without ensuring the isolation switch was
bypassed, resulting in an unplanned isolation of the RCIC system.  Because this issue is
of very low safety significance (Green) and was entered into CENG's CAP as CR-2013-002461, this violation is being treated as an NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy.  (NCV 05000410/2013003-01, Failure to Follow Containment Isolation System Surveillance Procedure Resulting in Isolation of the Reactor Coolant Isolation Cooling System)
 
20  Enclosure Cornerstone:  Emergency Preparedness
1EP4 Emergency Action Level and Emergency Plan Changes (71114.04 - 1 sample)
  a. Inspection Scope
  The Office of Nuclear Security and Incident Response headquarters'
staff performed an in-office review of the latest revisions of various emergency plan implementing
procedures and the emergency plan located under ADAMS accession number ML131071146 as listed in the Attachment.
CENG determined that in accordance with 10 CFR 50.54(q), the changes made in the
revisions resulted in no reduction in the effectiveness of the plan and that the revised
plan continued to meet the requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR Part 50.  The NRC review was not documented in a safety evaluation report and did not constitute approval of CENG-generated changes; therefore, this revision is subject to
future inspection.


  b. Findings
                                                16
  No findings were identified.  
    the information in the applicable licensing basis and/or design basis documents, and that
    the procedure had been properly reviewed and approved. The inspectors also
1EP6 Drill Evaluation (71114.06 - 1 sample)  
    witnessed the test or reviewed test data to verify that the test results adequately
   
    demonstrated restoration of the affected safety functions.
Training Observation
        Unit 1, Control room ventilation/smoke purge system test following installation of fire
    a. Inspection Scope
        damper BV-21-036 on April 3, 2013
  The inspectors observed a simulator training evolution for CENG's licensed operators on
        Unit 1, Power board 102 following National Fire Protection Act 805 modification on
        April 28, 2013
        Unit 1, Isolation valve IV-39-10R following control circuit stop relay replacement on
        May 9, 2013
        Unit 1, Replacement of excess flow check valve CKV-32-138 on May 10, 2013
        Unit 1, IV-29-07R diagnostic testing following body-to-bonnet seal replacement on
        May 23, 2013
b. Findings
    No findings were identified.
1R20 Refueling and Other Outage Activities (71111.20 - 1 sample)
  a. Inspection Scope
    The inspectors reviewed the stations work schedule and outage risk plan for the Unit 1
    maintenance and refueling outage (N1R22) which was conducted April 14 through May
    15, 2013. The inspectors reviewed CENGs development and implementation of outage
    plans and schedules to verify that risk, industry experience, previous site-specific
    problems, and defense-in-depth were considered. During the outage, the inspectors
    observed portions of the shutdown and cooldown processes and monitored controls
    associated with the following outage activities:
        Configuration management, including maintenance of defense-in-depth,
        commensurate with the outage plan for the key safety functions and compliance with
        the applicable TSs when taking equipment out of service
        Implementation of clearance activities and confirmation that tags were properly hung
        and that equipment was appropriately configured to safely support the associated
        work or testing
        Installation and configuration of reactor coolant pressure, level, and temperature
        instruments to provide accurate indication and instrument error accounting
        Status and configuration of electrical systems and switchyard activities to ensure that
        TSs were met
        Monitoring of decay heat removal operations
        Impact of outage work on the ability of the operators to operate the SFP cooling
        system
        Reactor water inventory controls, including flow paths, configurations, alternative
        means for inventory additions, and controls to prevent inventory loss
        Activities that could affect reactivity
        Maintenance of secondary containment as required by TSs
        Refueling activities
        Fatigue management
                                                                                      Enclosure


April 2, 2013, which required emergency plan implementation by an operations crew.  The inspectors observed Unit 1 licensed operator performance during an evaluated simulator scenario that included a loss of condenser vacuum, a stuck open ERV, and an
                                                17
anticipated transient without scram.  CENG planned for this evolution to be evaluated
        Tracking of startup prerequisites, walkdown of the drywell (primary containment) to
and included in performance indicator data regarding drill and exercise performance.
          verify that debris had not been left which could block the emergency core cooling
The inspectors observed event classification and notification activities performed by the
          system suction strainers, and startup and ascension to full power
crew. The focus of the inspectors' activities was to note any weaknesses and deficiencies in the crew's performance and ensure that CENG evaluators noted the same issues and entered them into the CAP.  
        Identification and resolution of problems related to refueling activities
  b. Findings
b.  Findings
  No findings were identified.
    No findings were identified.
 
1R22 Surveillance Testing (71111.22 - 8 samples)
 
aInspection Scope
    The inspectors observed performance of surveillance tests and/or reviewed test data of
    selected risk-significant SSCs to assess whether test results satisfied TSs, the UFSAR,
 
    and CENG procedure requirements. The inspectors verified that test acceptance criteria
21  Enclosure 2. RADIATION SAFETY
    were clear, tests demonstrated operational readiness and were consistent with design
  Cornerstone:  Public Radiation Safety and Occupational Radiation Safety 
    documentation, test instrumentation had current calibrations and the range and accuracy
  2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01)  
    for the application, tests were performed as written, and applicable test prerequisites
    were satisfied. Upon test completion, the inspectors considered whether the test results
  a. Inspection Scope
    supported that equipment was capable of performing the required safety functions. The
  From April 22 to 25, 2013, the inspectors reviewed and assessed CENG's performance in assessing the radiological hazards and exposure control in the workplace associated with licensed activities and the implementation of appropriate monitoring and exposure
    inspectors reviewed the following surveillance tests:
control measures for both individual and collective exposures.
        N1-ST-Q3, Unit 1, High-Pressure Coolant Injection Pump and Check Valve
          Operability Test for Train 12 on April 1, 2013
        N1-ST-C5, Unit 1, Secondary Containment and Reactor Building Emergency
          Ventilation System Operability Test for Loop 11 on April 8, 2013
        N1-ISP-LRT-TYC, Unit 1, Local Leak Rate Test for Valves IV-201-09 and IV-201-10
          on April 9, 2013
        N2-ISP-LDS-Q010, Unit 2, Reactor Building General Area Temperature Instrument
          Channel Functional Test on April 18, 2013
        Unit 2, RCS Leakage Determination Surveillance and Calculations on April 24, 2013
        N2-CSP-GEN-D100, Unit 2, Reactor Water/Auxiliary Water Chemistry Surveillance
          on April 24, 2013
        N1-TSP-201-001, Unit 1, Integrated Leak Rate Test of Primary Containment Type A
          Test on May 8, 2013
        N1-ST-Q15, Unit 1, Condensate Transfer System Operability Test on May 30, 2013
  bFindings
    Introduction. A self-revealing Green NCV of TS 5.4.1, Procedures, was identified at
    Unit 2 when a CENG I&C technician did not properly implement procedure N2-ISP-LDS-
    Q010, Reactor Building General Area Temperature Instrument Channel Functional
    Test, Revision 00102. As a result, a RHR/RCIC isolation bypass switch was
    inadvertently left in the NORMAL position during surveillance testing resulting in an
    unplanned RCIC isolation.
    Description. The RCIC system is designed to provide adequate makeup water to the
    reactor pressure vessel (RPV) automatically or manually following an RPV isolation
    accompanied by a loss of coolant flow from the feedwater system. In the event the
                                                                                      Enclosure


                                          18
The inspectors interviewed the radiation protection manager, radiation protection supervisors, radiation protection technicians (RPTs), and radiation workers. The inspectors performed walkdowns of various portions of the plant, performed independent
steam piping to the RCIC pump system leaks, temperature sensors in the RCIC pump
radiation dose rate measurements, observed work activities in radiological control areas, and reviewed CENG documents during the N1R22 outage. The inspectors used the  
room will close isolation valves in the RCIC system stopping the leak. CENG
requirements in 10 CFR 20, guidance in Regulatory Guide (RG) 8.38, "Control of Access to High and Very High Radiation Areas of Nuclear Plants," TSs, and CENG's procedures required by TSs as criteria for determining compliance.
surveillance procedure N2-ISP-LDS-Q010 is a TS surveillance test that verifies that the
group 5 (RHR) and group 10 (RCIC) isolation trip signals will close the respective
system isolation valves if a high-temperature condition occurs. The procedure tests this
function by simulating a high temperature condition and verifying correct system
response. Actual valve movement during testing is prevented by control room operators
blocking the test signal.
On April 2, 2013, an unplanned RCIC isolation occurred when I&C technicians did not
properly implement procedure N2-ISP-LDS-Q010 to block the test signal. Specifically,
step 7.2.1 required I&C technicians to request control room operators to place channel
bypass switch E31A-S4B RHR/RCIC ISOLATION BYPASS in BYPASS and to verify the
circuit was bypassed by observing annunciator and plant computer alarms prior to lifting
thermocouple leads in the field. This was not accomplished which resulted in the
isolation of the RCIC system.
Prior to the event, a pre-job brief was conducted by CENG I&C technicians performing
the work which focused on the roles and responsibilities of personnel including the lifting
of thermocouple leads safely and error free. Placing the RHR/RCIC isolation bypass
switch in BYPASS was not identified as a critical step, and no critical steps were
annotated in the work document as required by CNG-PR-1.01-1009, Procedure and
Work Order Use and Adherence Requirements, Revision 00701. However, the
requirement for operations personnel to place the isolation switch in BYPASS was
discussed during the procedure review with the control room supervisor who assigned a
control room operator to perform the task when requested by I&C technicians. Section
3.12 of CNG-PR-1.01-1009 defines place-keeping as physically marking steps to
prevent the omission or duplication of the steps to maintain an accounting of steps in
progress, steps completed, steps not applicable, and steps not yet performed. It lists
among high-risk practices to be avoided by signing or checking off a step as completed
before it is completed. After commencing surveillance procedure N2-ISP-LDS-Q010,
technicians used improper self-checking and place-keeping by checking and initialing as
complete step 7.2.1 to request operators to place the RHR/RCIC isolation bypass switch
in BYPASS and to verify annunciator and computer alarm points were in alarm without
that step having been performed. Consequently, when thermocouple leads were lifted in
the following step, a false high-temperature signal was generated resulting in the closing
of RCIC steam supply isolation valves 2ICS*MOV121, 2ICS*MOV128, 2ICS*MOV170,
and an unplanned isolation of RCIC. The surveillance test was immediately stopped, the
required TS action statements were entered for the RCIC system, and the system was
restored to an operable status after approximately 6 hours. The isolation signal was also
sent to the RHR system for SDC supply and return valves and for reactor head spray
isolation valve which were already closed at power. There was no impact on operability
of low-pressure coolant injection or containment spray functions of RHR.
A CENG investigation concluded human error as the primary cause for the inadvertent
isolation of the RCIC system. A contributing cause was the failure to implement
adequate corrective actions following a similar RCIC isolation event in 2007. Immediate
corrective actions for this event included a human performance stand down that
reinforced use of human performance tools and the need to identify and mark critical
steps during pre-job briefs, retraining the I&C technicians involved in the event on proper
use of human performance error prevention techniques, and improving bypass switch
                                                                                  Enclosure


                                            19
Inspection Planning
verification steps for procedure N2-ISP-LDS-Q010 and other similar leak detection
 
system surveillance procedures. CENG entered this issue in their CAP as CR-2013-
The inspectors reviewed the results of radiation protection program audits. The inspectors reviewed reports of operational occurrences related to occupational radiation safety since the last inspection on March 21, 2013.  
002461.
Analysis. The inspectors determined that CENGs failure to correctly implement
surveillance test procedure N2-ISP-LDS-Q010 was a performance deficiency that was
within CENGs ability to foresee and correct and should have been prevented. This
finding is more than minor because it is associated with the human performance attribute
of the Mitigating Systems cornerstone and affected the cornerstone objective to ensure
the availability, reliability, and capability of systems that respond to initiating events to
prevent undesirable consequences (i.e., core damage). Specifically, the inadvertent
isolation rendered the RCIC system inoperable and unable to perform its function for
approximately 6 hours. Additionally, this finding is similar to Example 4.b. of IMC 0612,
Appendix E, Examples of Minor Issues, and is more than minor due to the procedural
error leading to a plant transient, i.e. an unplanned RCIC isolation.
In accordance with IMC 0609.04, Initial Characterization of Findings, and Exhibit 2 of
IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power,
issued June 19, 2012, this finding represents a loss of safety function. Unit 2 is a
BWR-5, and as a result, RCIC is treated as having a separate high- pressure injection
safety function. A detailed analysis was conducted using SAPHIRE Version 8.0.8.0 and
Unit 2 SPAR Model 8.17. Using an exposure period of 6 hours and conservatively
assuming no recovery of the failed equipment, this finding had a change in core damage
frequency of low E-8. The dominant accident sequence was a grid- related loss of off-
site power with a failure of Division III power and the failure to recover off-site power and
the EDGs in 30 minutes. Since the change in core damage frequency was less than
1E-7, contributions from large early release and external event did not need to be
considered. Therefore, this finding was determined to be of very low safety significance
(Green).
This finding had a cross-cutting aspect in the area of Human Performance, Work
Practices, because the I&C technicians did not effectively employ self-checking and
place-keeping when implementing N2-ISP-LDS-Q010 which directly contributed to the
resulting procedural error [H.4(a)].
Enforcement. TS 5.4.1, Procedures, requires written procedures to be established,
implemented, and maintained covering the applicable procedures recommended in
Regulatory Guide (RG) 1.33, Quality Assurance Program Requirements (Operation),
Appendix A, Revision 2, dated February 1978. Section 8.b(2)(b) of RG 1.33 requires, in
part, specific procedures for surveillance tests on containment isolation. CENG
surveillance test procedure N2-ISP-LDS-Q010, Reactor Building General Area
Temperature Instrument Channel Functional Test, directed that the RHR/RCIC
ISOLATION BYPASS switch be placed in BYPASS to prevent an inadvertent
containment isolation while lifting thermocouple leads. Contrary to above, on April 2,
2013, technicians lifted thermocouple leads without ensuring the isolation switch was
bypassed, resulting in an unplanned isolation of the RCIC system. Because this issue is
of very low safety significance (Green) and was entered into CENGs CAP as CR-2013-
002461, this violation is being treated as an NCV, consistent with Section 2.3.2 of the
NRC Enforcement Policy. (NCV 05000410/2013003-01, Failure to Follow
Containment Isolation System Surveillance Procedure Resulting in Isolation of the
Reactor Coolant Isolation Cooling System)
                                                                                      Enclosure


   
                                                20
Radiological Hazard Assessment
    Cornerstone: Emergency Preparedness
  The inspectors conducted walkdowns and independent radiation measurements to evaluate material, work and radiological conditions in the facility including the drywell,
1EP4 Emergency Action Level and Emergency Plan Changes (71114.04 - 1 sample)
RB, refueling floor, and turbine building (TB).  
a.  Inspection Scope
    The Office of Nuclear Security and Incident Response headquarters staff performed an
    in-office review of the latest revisions of various emergency plan implementing
    procedures and the emergency plan located under ADAMS accession number
    ML131071146 as listed in the Attachment.
    CENG determined that in accordance with 10 CFR 50.54(q), the changes made in the
    revisions resulted in no reduction in the effectiveness of the plan and that the revised
    plan continued to meet the requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR
    Part 50. The NRC review was not documented in a safety evaluation report and did not
    constitute approval of CENG-generated changes; therefore, this revision is subject to
    future inspection.
b. Findings
    No findings were identified.
1EP6 Drill Evaluation (71114.06 - 1 sample)
    Training Observation
a.  Inspection Scope
    The inspectors observed a simulator training evolution for CENGs licensed operators on
    April 2, 2013, which required emergency plan implementation by an operations crew.
    The inspectors observed Unit 1 licensed operator performance during an evaluated
    simulator scenario that included a loss of condenser vacuum, a stuck open ERV, and an
    anticipated transient without scram. CENG planned for this evolution to be evaluated
    and included in performance indicator data regarding drill and exercise performance.
    The inspectors observed event classification and notification activities performed by the
    crew. The focus of the inspectors activities was to note any weaknesses and
    deficiencies in the crews performance and ensure that CENG evaluators noted the
    same issues and entered them into the CAP.
b.  Findings
    No findings were identified.
                                                                                      Enclosure


   
                                              21
The inspectors selected the following radiological risk-significant work activities that  
2.  RADIATION SAFETY
involved exposure to radiation:  
    Cornerstone: Public Radiation Safety and Occupational Radiation Safety
  Refueling floor activities Drywell control rod drive under-vessel work Drywell scaffolding Drywell ISI RWCU valve repairs  
2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01)
  a.  Inspection Scope
For these work activities, the inspectors assessed whether the pre-work surveys  
    From April 22 to 25, 2013, the inspectors reviewed and assessed CENGs performance
performed were appropriate to identify and quantify the radiological hazard and to establish adequate protective measures. The inspectors evaluated the radiological  
    in assessing the radiological hazards and exposure control in the workplace associated
survey program to determine if radiological hazards were properly identified.  
    with licensed activities and the implementation of appropriate monitoring and exposure
    control measures for both individual and collective exposures.
The inspectors observed work in potential airborne radioactivity areas and evaluated  
    The inspectors interviewed the radiation protection manager, radiation protection
whether the air samples from under the reactor vessel, from the reactor cavity and for
    supervisors, radiation protection technicians (RPTs), and radiation workers. The
22  Enclosure entries into the tent for repair of the SFP gate, were representative of the breathing air
    inspectors performed walkdowns of various portions of the plant, performed independent
zone and were properly evaluated.  The inspectors evaluated whether continuous air monitors on the refueling floor in the RB and at the drywell entrance were located to ensure appropriate detection sensitivity and were representative of actual work areas.  The inspectors evaluated CENG's program fo
    radiation dose rate measurements, observed work activities in radiological control areas,
r monitoring levels of loose surface contamination in areas of the plant.
    and reviewed CENG documents during the N1R22 outage. The inspectors used the
    requirements in 10 CFR 20, guidance in Regulatory Guide (RG) 8.38, Control of Access
    to High and Very High Radiation Areas of Nuclear Plants, TSs, and CENGs procedures
    required by TSs as criteria for determining compliance.
    Inspection Planning
    The inspectors reviewed the results of radiation protection program audits. The
    inspectors reviewed reports of operational occurrences related to occupational radiation
    safety since the last inspection on March 21, 2013.
    Radiological Hazard Assessment
    The inspectors conducted walkdowns and independent radiation measurements to
    evaluate material, work and radiological conditions in the facility including the drywell,
    RB, refueling floor, and turbine building (TB).
    The inspectors selected the following radiological risk-significant work activities that
    involved exposure to radiation:
        Refueling floor activities
        Drywell control rod drive under-vessel work
        Drywell scaffolding
        Drywell ISI
        RWCU valve repairs
    For these work activities, the inspectors assessed whether the pre-work surveys
    performed were appropriate to identify and quantify the radiological hazard and to
    establish adequate protective measures. The inspectors evaluated the radiological
    survey program to determine if radiological hazards were properly identified.
    The inspectors observed work in potential airborne radioactivity areas and evaluated
    whether the air samples from under the reactor vessel, from the reactor cavity and for
                                                                                        Enclosure


                                          22
entries into the tent for repair of the SFP gate, were representative of the breathing air
zone and were properly evaluated. The inspectors evaluated whether continuous air
monitors on the refueling floor in the RB and at the drywell entrance were located to
ensure appropriate detection sensitivity and were representative of actual work areas.
The inspectors evaluated CENGs program for monitoring levels of loose surface
contamination in areas of the plant.
Instructions to Workers
Instructions to Workers
  The inspectors reviewed the following radiation work permits (RWPs) used to access high radiation areas and evaluated if the specified work control instructions and control  
The inspectors reviewed the following radiation work permits (RWPs) used to access
barriers were consistent with TS requirements for locked high radiation areas:  
high radiation areas and evaluated if the specified work control instructions and control
 
barriers were consistent with TS requirements for locked high radiation areas:
  RWP 113330H, RB 261 RWCU Valve Work RWP 113802H, Drywell Under-Vessel Work RWP 113890A, RB 340 Reactor Disassembly and Reassembly RWP 113890B, RB 340 Underwater Work on Refuel Floor RWP 113890E, RB 340 Reactor Cavity and Equipment Storage Pit Decon RWP 113806H, Drywell ISI RWP 113815, RB 261 Flow Accelerated Corrosion (FAC) ISI RWP 113810, Drywell General Scaffolding Activities  
  RWP 113330H, RB 261 RWCU Valve Work
The inspectors assessed whether permissible dose for radiological-significant work under each RWP was clearly identified. The  
  RWP 113802H, Drywell Under-Vessel Work
inspectors evaluated whether electronic personal dosimeter alarm set points were in conformance with survey indications and plant procedural requirements.  
  RWP 113890A, RB 340 Reactor Disassembly and Reassembly
  RWP 113890B, RB 340 Underwater Work on Refuel Floor
The inspectors reviewed CR-2013-002474 and CR-2012-002974 for occurrences where  
  RWP 113890E, RB 340 Reactor Cavity and Equipment Storage Pit Decon
a worker's electronic personal dosimeter noticeably malfunctioned or alarmed. The  
  RWP 113806H, Drywell ISI
inspectors evaluated whether workers responded appropriately to the off-normal condition. The inspectors assessed whether the issue was included in the CAP and whether compensatory dose evaluations were conducted.  
  RWP 113815, RB 261 Flow Accelerated Corrosion (FAC) ISI
 
  RWP 113810, Drywell General Scaffolding Activities
The inspectors assessed whether permissible dose for radiological-significant work
For work activities that could suddenly and severely increase radiological conditions, i.e.,  
under each RWP was clearly identified. The inspectors evaluated whether electronic
upper elevation of drywell during spent fuel movement and low power range monitor  
personal dosimeter alarm set points were in conformance with survey indications and
moves, the inspectors assessed CENG's means to inform workers of these changes that could significantly impact their occupational dose.  
plant procedural requirements.
The inspectors reviewed CR-2013-002474 and CR-2012-002974 for occurrences where
a workers electronic personal dosimeter noticeably malfunctioned or alarmed. The
inspectors evaluated whether workers responded appropriately to the off-normal
condition. The inspectors assessed whether the issue was included in the CAP and
whether compensatory dose evaluations were conducted.
For work activities that could suddenly and severely increase radiological conditions, i.e.,
upper elevation of drywell during spent fuel movement and low power range monitor
moves, the inspectors assessed CENGs means to inform workers of these changes that
could significantly impact their occupational dose.
Contamination and Radioactive Material Control
Contamination and Radioactive Material Control
 
The inspectors observed the access control point where CENG monitors potentially
The inspectors observed the access control point where CENG monitors potentially contaminated material leaving the radiological control area and inspected the methods used for control, survey, and release from these areas. The inspectors observed the
contaminated material leaving the radiological control area and inspected the methods
 
used for control, survey, and release from these areas. The inspectors observed the
performance of personnel surveying and releasing material for unrestricted use and
evaluated whether the release surveys were performed in accordance with plant
performance of personnel surveying and releasing material for unrestricted use and  
procedures and process knowledge concerning the equipment.
evaluated whether the release surveys were performed in accordance with plant procedures and process knowledge concerning the equipment.  
                                                                                  Enclosure
 
23  Enclosure Radiological Hazards Control and Work Coverage
 
The inspectors evaluated ambient radiological conditions and performed independent radiation measurements during plant walkdowns.  The inspectors assessed whether the conditions were consistent with applicable posted surveys, RWPs, and associated
 
worker briefings.
 
The inspectors assessed whether radiation monitoring devices were placed on the
individual's body consistent with CENG procedures.  The inspectors assessed whether the dosimeter was placed in the location of highest expected dose and that CENG properly implemented an NRC-approved method of determining effective dose
 
equivalent.
 
The inspectors reviewed the application of dosimetry to effectively monitor exposure to personnel in high radiation work areas with significant dose rate gradients; e.g., RWCU repairs and workers under vessel in the control rod drive area.


                                          23
The inspectors reviewed the following RWPs for work within airborne radioactivity areas with the potential for individual worker internal exposures:  
Radiological Hazards Control and Work Coverage
  RWP 113802H, Under-Vessel Control Rod Drive Work RWP 113330H, RWCU Valve Work RWP 113890E, RB 340 Reactor Cavity and Equipment Storage Pit Decontamination  
The inspectors evaluated ambient radiological conditions and performed independent
radiation measurements during plant walkdowns. The inspectors assessed whether the
The inspectors evaluated airborne radioactive controls and monitoring including potential  
conditions were consistent with applicable posted surveys, RWPs, and associated
for significant airborne levels. The inspectors assessed applicable containment barriers integrity and the operation of temporary high-efficiency particulate air ventilation system.  
worker briefings.
The inspectors assessed whether radiation monitoring devices were placed on the
individuals body consistent with CENG procedures. The inspectors assessed whether
the dosimeter was placed in the location of highest expected dose and that CENG
properly implemented an NRC-approved method of determining effective dose
equivalent.
The inspectors reviewed the application of dosimetry to effectively monitor exposure to
personnel in high radiation work areas with significant dose rate gradients; e.g., RWCU
repairs and workers under vessel in the control rod drive area.
The inspectors reviewed the following RWPs for work within airborne radioactivity areas
with the potential for individual worker internal exposures:
  RWP 113802H, Under-Vessel Control Rod Drive Work
  RWP 113330H, RWCU Valve Work
  RWP 113890E, RB 340 Reactor Cavity and Equipment Storage Pit Decontamination
The inspectors evaluated airborne radioactive controls and monitoring including potential
for significant airborne levels. The inspectors assessed applicable containment barriers
integrity and the operation of temporary high-efficiency particulate air ventilation system.
Risk-Significant High Radiation Area and Very High Radiation Area Controls
Risk-Significant High Radiation Area and Very High Radiation Area Controls
 
The inspectors discussed the controls and procedures for high risk high radiation areas
The inspectors discussed the controls and procedures for high risk high radiation areas and very high radiation areas with the radiation protection manager. The inspectors discussed with first-line health physics supervisors the controls in place for special areas  
and very high radiation areas with the radiation protection manager. The inspectors
that have the potential to become very high radiation areas during refueling outages.
discussed with first-line health physics supervisors the controls in place for special areas
The inspectors evaluated the controls for very high radiation areas and areas with the  
that have the potential to become very high radiation areas during refueling outages.
potential to become a very high radiation area to ensure that an individual was not able  
The inspectors evaluated the controls for very high radiation areas and areas with the
to gain unauthorized access to these areas.  
potential to become a very high radiation area to ensure that an individual was not able
Radiation Worker Performance
to gain unauthorized access to these areas.
 
Radiation Worker Performance
The inspectors observed the performance of radiation workers during the N1R22 with  
The inspectors observed the performance of radiation workers during the N1R22 with
respect to stated radiation protection work requirements. The inspectors assessed whether workers were aware of the radiological conditions in their workplace, the RWP controls and limits, and whether their behavior reflected the level of radiological hazards  
respect to stated radiation protection work requirements. The inspectors assessed
present.  
whether workers were aware of the radiological conditions in their workplace, the RWP
controls and limits, and whether their behavior reflected the level of radiological hazards
present.
Radiation Protection Technician Proficiency
Radiation Protection Technician Proficiency
  The inspectors observed the performance of the RPTs during the N1R22 with respect to controlling radiation work. The inspectors evaluated whether technicians were aware of
The inspectors observed the performance of the RPTs during the N1R22 with respect to
24  Enclosure the radiological conditions in their workplace, the RWP controls and limits, and whether their behavior was consistent with their training and qualifications with respect to the
controlling radiation work. The inspectors evaluated whether technicians were aware of
radiological hazards and work activities.
                                                                                  Enclosure
Problem Identification and Resolution
 
The inspectors evaluated whether problems associated with radiation monitoring and
exposure control were being identified by
CENG at an appropriate threshold and were properly addressed for resolution in the CENG's CAP.  The inspectors assessed the appropriateness of the corrective actions for a selected sample of problems documented by CENG that involved radiation monitoring and exposure controls.  The inspectors assessed CENG's process for applying operating experience to their plant.
  b. Findings
  No findings were identified.


   
                                              24
2RS2 Occupational ALARA Planning and Controls (71124.02)   
    the radiological conditions in their workplace, the RWP controls and limits, and whether
  a. Inspection Scope
    their behavior was consistent with their training and qualifications with respect to the
  The inspectors assessed performance with respect to maintaining occupational  
    radiological hazards and work activities.
individual and collective radiation exposures as low as reasonably achievable (ALARA)  
    Problem Identification and Resolution
during the N1R22. The inspectors used the requirements in 10 CFR 20, RG 8.8,  
    The inspectors evaluated whether problems associated with radiation monitoring and
"Information Relevant to Ensuring that Occupational Radiation Exposures at Nuclear Power Stations will be As Low As Is Reasonably Achievable," RG 8.10, "Operating  
    exposure control were being identified by CENG at an appropriate threshold and were
Philosophy for Maintaining Occupational Radiation Exposures As Low As Is Reasonably Achievable," TSs, and CENG's procedures required by TSs as criteria for determining compliance.  
    properly addressed for resolution in the CENGs CAP. The inspectors assessed the
    appropriateness of the corrective actions for a selected sample of problems documented
    by CENG that involved radiation monitoring and exposure controls. The inspectors
    assessed CENGs process for applying operating experience to their plant.
b. Findings
    No findings were identified.
2RS2 Occupational ALARA Planning and Controls (71124.02)
  a. Inspection Scope
    The inspectors assessed performance with respect to maintaining occupational
    individual and collective radiation exposures as low as reasonably achievable (ALARA)
    during the N1R22. The inspectors used the requirements in 10 CFR 20, RG 8.8,
    Information Relevant to Ensuring that Occupational Radiation Exposures at Nuclear
    Power Stations will be As Low As Is Reasonably Achievable, RG 8.10, Operating
    Philosophy for Maintaining Occupational Radiation Exposures As Low As Is Reasonably
    Achievable, TSs, and CENGs procedures required by TSs as criteria for determining
    compliance.
    Inspection Planning
    The inspectors reviewed pertinent information regarding CENGs collective dose history,
    current exposure trends, and ongoing or planned activities in order to assess current
    performance and exposure challenges.
    The inspectors reviewed changes in the radioactive source term by reviewing the trend
    in average contact dose rates on reactor recirculation piping for the time period between
    1984 and the present Unit 1 outage. The inspectors reviewed ALARA procedures that
    specified the processes used to estimate and track exposures for radiological work
    activities.
    Radiological Work Planning
    The inspectors selected the following work activities that had the highest exposure
    significance:
        ALARA Plan 2013-1-002, Drywell Under-Vessel Activities and Associated Activities
        N1R22
        ALARA Plan 2013-1-004, Drywell Operations and Local Leak Rate Test Activities
                                                                                        Enclosure


Inspection Planning
                                          25
 
  ALARA Plan 2013-1-006, Drywell ISI Activities
The inspectors reviewed pertinent information regarding CENG's collective dose history,
  ALARA Plan 2013-1-007, Recirculation Pump Seals Replacement and Motor PMs
current exposure trends, and ongoing or planned activities in order to assess current
    (Numbers 11, 13, and 15)
performance and exposure challenges.
  ALARA Plan 2013-1-010, Drywell Scaffold Activities
 
  ALARA Plan 2013-1-014, Drywell Emergency Relief Valve and Pilot Valve Work
The inspectors reviewed changes in the radioactive source term by reviewing the trend in average contact dose rates on reactor recirculation piping for the time period between
    Activities
1984 and the present Unit 1 outage.  The inspectors reviewed ALARA procedures that
  ALARA Plan 2013-1-024, Main Steam Isolation Valve 01-02 Stem Replacement
specified the processes used to estimate and track exposures for radiological work
    Actuator Remove/Replace and Testing
activities. 
  ALARA Plan 2013-1-029, Balance of Plant FAC Activities in RWCU Heat Exchanger
Radiological Work Planning
    Room and Valve Aisles
 
  ALARA Plan 2013-1-030, Refuel Floor Activities
The inspectors selected the following work activities that had the highest exposure
  ALARA Plan 2013-1-031, RWCU Miscellaneous Maintenance, Preventive
significance:
    Maintenance, Surveillance Testing, Operations N1R22
 
The inspectors reviewed the ALARA work activity evaluations, exposure estimates, and
  ALARA Plan 2013-1-002, Drywell Under-Vessel Activities and Associated Activities N1R22  ALARA Plan 2013-1-004, Drywell Operations and Local Leak Rate Test Activities 
exposure reduction requirements. The inspectors determined whether CENG
25  Enclosure  ALARA Plan 2013-1-006, Drywell ISI Activities ALARA Plan 2013-1-007, Recirculation Pump Seals Replacement and Motor PMs (Numbers 11, 13, and 15)   ALARA Plan 2013-1-010, Drywell Scaffold Activities ALARA Plan 2013-1-014, Drywell Emergency Relief Valve and Pilot Valve Work  
reasonably grouped the radiological work into work activities based on historical
Activities ALARA Plan 2013-1-024, Main Steam Isolation Valve 01-02 Stem Replacement Actuator Remove/Replace and Testing ALARA Plan 2013-1-029, Balance of Plant FAC
precedence, industry norms, and/or special circumstances.
Activities in RWCU Heat Exchanger  
The inspectors assessed when CENGs planning identified appropriate dose reduction
Room and Valve Aisles ALARA Plan 2013-1-030, Refuel Floor Activities ALARA Plan 2013-1-031, RWCU Miscellaneous Maintenance, Preventive  
techniques, considered alternate dose reduction features, and estimated reasonable
Maintenance, Surveillance Testing, Operations N1R22  
dose goals. The inspectors evaluated whether the ALARA assessment had taken into
The inspectors reviewed the ALARA work activity evaluations, exposure estimates, and exposure reduction requirements. The inspectors determined whether CENG  
account decreased worker efficiency from use of respiratory protective devices and/or
reasonably grouped the radiological work into work activities based on historical  
heat stress mitigation equipment. The inspectors determined whether work planning
precedence, industry norms, and/or special circumstances.  
considered the use of remote technologies as a means to reduce dose and the use of
 
dose reduction insights from industry operating experience and plant-specific lessons
The inspectors assessed when CENG's planning identified appropriate dose reduction techniques, considered alternate dose reduction features, and estimated reasonable  
learned. The inspectors assessed the integration of ALARA requirements into work
dose goals. The inspectors evaluated whether the ALARA assessment had taken into  
procedure and RWP documents.
account decreased worker efficiency from use of respiratory protective devices and/or  
heat stress mitigation equipment. The inspectors determined whether work planning considered the use of remote technologies as a means to reduce dose and the use of dose reduction insights from industry operating experience and plant-specific lessons  
learned. The inspectors assessed the integration of ALARA requirements into work  
procedure and RWP documents.  
 
Verification of Dose Estimates and Exposure Tracking Systems
Verification of Dose Estimates and Exposure Tracking Systems
  The inspectors reviewed the assumptions and basis for the current annual collective  
The inspectors reviewed the assumptions and basis for the current annual collective
dose estimate and outage collective dose estimate for accuracy. The inspectors  
dose estimate and outage collective dose estimate for accuracy. The inspectors
reviewed applicable procedures to determine the methodology for estimating exposures  
reviewed applicable procedures to determine the methodology for estimating exposures
from specific work activities and for department and station collective dose goals.  
from specific work activities and for department and station collective dose goals.
The inspectors evaluated whether CENG had established measures to track, trend, and  
The inspectors evaluated whether CENG had established measures to track, trend, and
reduce occupational doses for ongoing work activities. The inspectors assessed  
reduce occupational doses for ongoing work activities. The inspectors assessed
whether dose threshold criteria were established to prompt additional reviews and/or  
whether dose threshold criteria were established to prompt additional reviews and/or
additional ALARA planning and controls.  
additional ALARA planning and controls.
The inspectors evaluated CENG's method of adjusting exposure estimates or  
The inspectors evaluated CENGs method of adjusting exposure estimates or
re-planning work when unexpected changes in scope or emergent work were  
re-planning work when unexpected changes in scope or emergent work were
encountered. The inspectors assessed whether adjustments to exposure estimates  
encountered. The inspectors assessed whether adjustments to exposure estimates
were based on sound radiation protection and ALARA principles or if they were just  
were based on sound radiation protection and ALARA principles or if they were just
adjusted to account for failures to plan/control the work.  
adjusted to account for failures to plan/control the work.
 
                                                                                Enclosure
 
26  Enclosure  
Source Term Reduction and Control
 
The inspectors used station records to determine the historical trends and current status of plant source term known to contribute to elevated facility collective exposure.  The inspectors assessed whether CENG had made allowances or developed contingency
plans for expected changes in the source term as the result of changes in plant fuel
performance issues or changes in plant primary chemistry. 
 
Radiation Worker Performance
  The inspectors observed radiation workers and RPTs performance during refueling
outage activities in radiation areas, airborne radioactivity areas, and high radiation areas. 
The inspectors evaluated whether workers demonstrated the ALARA philosophy in
practice and whether there were any procedure or RWP compliance issues.
Problem Identification and Resolution
 
The inspectors evaluated whether problems associated with ALARA planning and
controls were being identified by CENG at an appropriate threshold and were properly addressed for resolution in the CENG's CAP.
  b. Findings
 
No findings were identified.


  2RS3 In-Plant Airborne Radioactivity Control and Mitigation
                                              26
(71124.03)  
    Source Term Reduction and Control
    a. Inspection Scope
    The inspectors used station records to determine the historical trends and current status
  This area was inspected to verify in-plant airborne concentrations were being controlled consistent with ALARA principles and the use of respiratory protection devices on-site does not pose an undue risk to the wearer. The inspectors used the requirements in  
    of plant source term known to contribute to elevated facility collective exposure. The
10 CFR 20, the guidance in RG 8.15, "Acceptable Programs for Respiratory Protection,"
    inspectors assessed whether CENG had made allowances or developed contingency
RG 8.25, "Air Sampling in the Workplace," NUREG-0041, "Manual of Respiratory  
    plans for expected changes in the source term as the result of changes in plant fuel
Protection Against Airborne Radioactive Material," TSs, and CENG's procedures required by TSs as criteria for determining compliance.  
    performance issues or changes in plant primary chemistry.
Inspection Planning
    Radiation Worker Performance
 
    The inspectors observed radiation workers and RPTs performance during refueling
The inspectors reviewed the UFSAR to identify areas of the plant designed as potential  
    outage activities in radiation areas, airborne radioactivity areas, and high radiation areas.
airborne radiation areas and any associated ventilation systems or airborne monitoring instrumentation. This review included instruments used to identify changing airborne radiological conditions such that actions to prevent an overexposure may be taken. The  
    The inspectors evaluated whether workers demonstrated the ALARA philosophy in
review included an overview of the respiratory protection program and a description of  
    practice and whether there were any procedure or RWP compliance issues.
the types of devices used. The inspectors reviewed procedures for maintenance,  
    Problem Identification and Resolution
inspection, and use of respiratory protection equipment as well as procedures for  
    The inspectors evaluated whether problems associated with ALARA planning and
maintenance and testing of breathing air quality.  
    controls were being identified by CENG at an appropriate threshold and were properly
 
    addressed for resolution in the CENGs CAP.
b. Findings
 
    No findings were identified.
27  Enclosure Engineering Controls
2RS3 In-Plant Airborne Radioactivity Control and Mitigation (71124.03)
 
a. Inspection Scope
The inspectors reviewed CENG's use of permanent and temporary ventilation to
    This area was inspected to verify in-plant airborne concentrations were being controlled
determine whether CENG uses ventilation systems as part of its engineering controls to control airborne radioactivity.  The inspectors reviewed procedural guidance for use of
    consistent with ALARA principles and the use of respiratory protection devices on-site
installed plant systems to reduce dose and assessed whether the systems are used during high-risk activities.
    does not pose an undue risk to the wearer. The inspectors used the requirements in
    10 CFR 20, the guidance in RG 8.15, Acceptable Programs for Respiratory Protection,
    RG 8.25, Air Sampling in the Workplace, NUREG-0041, Manual of Respiratory
    Protection Against Airborne Radioactive Material, TSs, and CENGs procedures
    required by TSs as criteria for determining compliance.
    Inspection Planning
    The inspectors reviewed the UFSAR to identify areas of the plant designed as potential
    airborne radiation areas and any associated ventilation systems or airborne monitoring
    instrumentation. This review included instruments used to identify changing airborne
    radiological conditions such that actions to prevent an overexposure may be taken. The
    review included an overview of the respiratory protection program and a description of
    the types of devices used. The inspectors reviewed procedures for maintenance,
    inspection, and use of respiratory protection equipment as well as procedures for
    maintenance and testing of breathing air quality.
                                                                                        Enclosure


                                              27
The inspectors selected two temporary ventilation system setups on the refuel floor used to support work in contaminated areas. The inspectors assessed whether the use of these systems is consistent with procedural guidance and ALARA principles.  
    Engineering Controls
    The inspectors reviewed CENGs use of permanent and temporary ventilation to
    determine whether CENG uses ventilation systems as part of its engineering controls to
    control airborne radioactivity. The inspectors reviewed procedural guidance for use of
    installed plant systems to reduce dose and assessed whether the systems are used
    during high-risk activities.
    The inspectors selected two temporary ventilation system setups on the refuel floor used
    to support work in contaminated areas. The inspectors assessed whether the use of
    these systems is consistent with procedural guidance and ALARA principles.
    The inspectors reviewed airborne monitoring protocols for the drywell and refueling floor
    continuous air monitors used to monitor and warn of changing airborne concentrations in
    the plant and evaluating whether the alarms and set points are sufficient to prompt
    worker action to ensure that doses are maintained within the limits of 10 CFR 20 and the
    ALARA concept.
    The inspectors assessed whether CENG had established threshold criteria for
    evaluating levels of airborne beta-emitting and alpha-emitting radionuclides.
    Use of Respiratory Protection Devices
    The inspectors selected RWCU repairs and under-vessel control rod drive work activities
    where respiratory protection devices were used to limit the intake of radioactive
    materials and assessed whether CENG performed an evaluation concluding that further
    engineering controls were not practical and that the use of respirators is ALARA. The
    inspectors also evaluated whether CENG had established means (such as routine
    bioassay) to determine if the level of protection (protection factor) provided by the
    respiratory protection devices during use was at least as good as that assumed in work
    controls and dose assessment.
    Problem Identification and Resolution
    The inspectors evaluated whether problems associated with the control and mitigation of
    in-plant airborne radioactivity were being identified by CENG at an appropriate threshold
    and were properly addressed for resolution in CENGs CAP. The inspectors assessed
    whether the corrective actions were appropriate for a selected sample of problems
    involving airborne radioactivity and were appropriately documented.
b.  Findings
    No findings were identified.
2RS4 Occupational Dose Assessment (71124.04)
a.  Inspection Scope
    From April 22 to 25, 2013, the inspectors reviewed occupational doses to ensure they
    were appropriately monitored and assessed. The inspectors used the requirements in
    10 CFR 20, RG 8.13, Instruction Concerning Prenatal Radiation Exposure, RG 8.36,
                                                                                        Enclosure


                                        28
The inspectors reviewed airborne monitoring protocols for the drywell and refueling floor
Radiation Dose to the Embryo/Fetus, RG 8.40, Methods for Measuring Effective Dose
continuous air monitors used to monitor and warn of changing airborne concentrations in the plant and evaluating whether the alarms and set points are sufficient to prompt worker action to ensure that doses are maintained within the limits of 10 CFR 20 and the
Equivalent from External Exposure, TSs, and CENGs procedures required by TSs as
ALARA concept. 
criteria for determining compliance.
 
Inspection Planning
The inspectors reviewed the results of Unit 1 radiation protection program audits related
The inspectors assessed whether CENG had established threshold criteria for evaluating levels of airborne beta-emitting and alpha-emitting radionuclides.
to internal and external dosimetry. A review was conducted of procedures associated
with dosimetry operations including issuance/use of external dosimetry, assessment of
Use of Respiratory Protection Devices
internal dose, and evaluation of and dose assessment for radiological incidents. The
 
inspectors evaluated whether CENG had established procedural requirements for
The inspectors selected RWCU repairs and under-vessel control rod drive work activities
determining when external dosimetry and internal dose assessments are required.
where respiratory protection devices were used to limit the intake of radioactive materials and assessed whether CENG performed an evaluation concluding that further engineering controls were not practical and that the use of respirators is ALARA.  The
inspectors also evaluated whether CENG had established means (such as routine
bioassay) to determine if the level of protection (protection factor) provided by the
respiratory protection devices during use was at least as good as that assumed in work controls and dose assessment.
Problem Identification and Resolution
 
The inspectors evaluated whether problems associated with the control and mitigation of
in-plant airborne radioactivity were being identified by CENG at an appropriate threshold and were properly addressed for resolution in CENG's CAP.  The inspectors assessed whether the corrective actions were appropriate for a selected sample of problems
involving airborne radioactivity and were appropriately documented.
 
  b. Findings
  No findings were identified.
 
2RS4 Occupational Dose Assessment
(71124.04)
 
  a. Inspection Scope
  From April 22 to 25, 2013, the inspectors reviewed occupational doses to ensure they
were appropriately monitored and assessed.  The inspectors used the requirements in
10 CFR 20, RG 8.13, "Instruction Concerning Prenatal Radiation Exposure," RG 8.36, 
28  Enclosure "Radiation Dose to the Embryo/Fetus," RG 8.40, "Methods for Measuring Effective Dose  
Equivalent from External Exposure," TSs, and CENG's procedures required by TSs as criteria for determining compliance.  
Inspection Planning
 
The inspectors reviewed the results of Unit 1 radiation protection program audits related  
to internal and external dosimetry. A review was conducted of procedures associated  
with dosimetry operations including issuance/use of external dosimetry, assessment of internal dose, and evaluation of and dose assessment for radiological incidents. The inspectors evaluated whether CENG had established procedural requirements for  
determining when external dosimetry and internal dose assessments are required.  
External Dosimetry
External Dosimetry
  The inspectors evaluated whether CENG's dosimetry vendor was accredited with the National Voluntary Laboratory Accredited Program and if the approved irradiation test  
The inspectors evaluated whether CENGs dosimetry vendor was accredited with the
categories for each type of personnel dosimeter used were consistent with the types and  
National Voluntary Laboratory Accredited Program and if the approved irradiation test
energies of the radiation present and the way the dosimeter is being used.  
categories for each type of personnel dosimeter used were consistent with the types and
The inspectors evaluated the onsite storage of dosimeters before issuance, during use,  
energies of the radiation present and the way the dosimeter is being used.
and before processing and reading. The inspectors also reviewed the guidance  
The inspectors evaluated the onsite storage of dosimeters before issuance, during use,
provided to radiation workers with respect to care and storage of dosimeters.  
and before processing and reading. The inspectors also reviewed the guidance
 
provided to radiation workers with respect to care and storage of dosimeters.
The inspectors assessed the use of electronic personal dosimeters to determine if
The inspectors assessed the use of electronic personal dosimeters to determine if CENG uses a correction factor to address the response of the electronic personal dosimeter as compared to the dosimeter of legal record for situations when the  
CENG uses a correction factor to address the response of the electronic personal
electronic personal dosimeter is used to assign dose and whether the correction factor is  
dosimeter as compared to the dosimeter of legal record for situations when the
based on sound technical principles.  
electronic personal dosimeter is used to assign dose and whether the correction factor is
The inspectors reviewed two CAP documents for adverse trends related to electronic personal dosimeters. The inspectors assessed whether CENG had identified any  
based on sound technical principles.
adverse trends and implemented appropriate corrective actions.  
The inspectors reviewed two CAP documents for adverse trends related to electronic
personal dosimeters. The inspectors assessed whether CENG had identified any
adverse trends and implemented appropriate corrective actions.
Internal Dosimetry
Internal Dosimetry
 
Routine Bioassay (In Vivo)
Routine Bioassay (In Vivo)
  The inspectors reviewed procedures used to assess the dose from internally deposited  
The inspectors reviewed procedures used to assess the dose from internally deposited
radionuclides using whole body counting equi
radionuclides using whole body counting equipment. The inspectors evaluated whether
pment. The inspectors evaluated whether the procedures addressed methods for differentiating between internal and external  
the procedures addressed methods for differentiating between internal and external
contamination, the release of contaminated individuals, determining the route of intake  
contamination, the release of contaminated individuals, determining the route of intake
and the assignment of dose.  
and the assignment of dose.
The inspectors reviewed CENGs evaluation for use of its portal radiation monitors as a
The inspectors reviewed CENG's evaluation for use of its portal radiation monitors as a  
passive monitoring system. The inspectors assessed if instrument minimum detectable
passive monitoring system. The inspectors assessed if instrument minimum detectable  
activities were adequate to determine the potential for internally deposited radionuclides
activities were adequate to determine the potential for internally deposited radionuclides  
sufficient to prompt an investigation.
sufficient to prompt an investigation.  
                                                                                Enclosure
 
 
29  Enclosure Special Bioassay (In Vitro)
 
There was no internal dose assessments obtained using whole body count results for the inspectors to review.  There was no internal dose assessments obtained using urinalysis or fecal sample results for the inspectors to review.


                                          29
The inspectors reviewed the vendor laboratory quality assurance program and assessed  
Special Bioassay (In Vitro)
whether the laboratory participated in an industry-recognized cross check program  
There was no internal dose assessments obtained using whole body count results for
including whether out-of-tolerance results were reviewed, evaluated, and resolved appropriately.  
the inspectors to review. There was no internal dose assessments obtained using
urinalysis or fecal sample results for the inspectors to review.
The inspectors reviewed the vendor laboratory quality assurance program and assessed
whether the laboratory participated in an industry-recognized cross check program
including whether out-of-tolerance results were reviewed, evaluated, and resolved
appropriately.
Internal Dose Assessment - Airborne Monitoring
Internal Dose Assessment - Airborne Monitoring
 
The inspectors reviewed CENGs program for dose assessment based on airborne
The inspectors reviewed CENG's program for dose assessment based on airborne monitoring and calculations of derived air concentration calculations. The inspectors determined whether flow rates and collection times for air sampling equipment were  
monitoring and calculations of derived air concentration calculations. The inspectors
adequate to allow appropriate lower limits of detection to be obtained. CENG had  
determined whether flow rates and collection times for air sampling equipment were
performed internal dose assessments using airborne/derived air concentration  
adequate to allow appropriate lower limits of detection to be obtained. CENG had
monitoring for some work in the cavity during the N1R22.  
performed internal dose assessments using airborne/derived air concentration
Internal Dose Assessment - Whole Body Count Analyses
monitoring for some work in the cavity during the N1R22.
 
Internal Dose Assessment - Whole Body Count Analyses
CENG has not documented any internal dose assessments using whole body count results during the period reviewed.  
CENG has not documented any internal dose assessments using whole body count
 
results during the period reviewed.
Special Dosimetry Situations
Special Dosimetry Situations
 
Declared Pregnant Workers
Declared Pregnant Workers
 
The inspectors assessed the process used by CENG to inform workers of the risks of
The inspectors assessed the process used by CENG to inform workers of the risks of radiation exposure to the embryo/fetus, the regulatory aspects of declaring a pregnancy, and the specific process to be used for monitoring and controlling exposure to a  
radiation exposure to the embryo/fetus, the regulatory aspects of declaring a pregnancy,
declared pregnant worker. CENG has not documented any internal dose assessments  
and the specific process to be used for monitoring and controlling exposure to a
for declared pregnant workers during this inspection period.  
declared pregnant worker. CENG has not documented any internal dose assessments
 
for declared pregnant workers during this inspection period.
Dosimeter Placement and Assessment of Effective Dose Equivalent for External
Dosimeter Placement and Assessment of Effective Dose Equivalent for External  
Exposures
Exposures
The inspectors reviewed CENGs methodology for monitoring external dose in non-
The inspectors reviewed CENG's methodology for monitoring external dose in non-
uniform radiation fields or where large dose gradients exist. The inspectors evaluated
uniform radiation fields or where large dose gradients exist. The inspectors evaluated  
CENGs criteria for determining when alternate monitoring such as use of multi-badging
CENG's criteria for determining when alternate monitoring such as use of multi-badging  
is to be implemented.
is to be implemented.  
The inspectors reviewed dose assessments performed for workers performing under-
The inspectors reviewed dose assessments performed for workers performing under-
vessel work and RWCU repairs. These workers used multi-badging to evaluate effective  
vessel work and RWCU repairs. These workers used multi-badging to evaluate effective
dose equivalent and the dose assessment was performed consistent with CENG  
dose equivalent and the dose assessment was performed consistent with CENG
procedures and dosimetry standards.  
procedures and dosimetry standards.
 
                                                                                Enclosure
 
30  Enclosure  
Shallow Dose Equivalent
 
There were no dose assessments for shallow dose equivalent available for review.  The inspectors evaluated CENG's method for calculating shallow dose equivalent from distributed skin contamination or discrete radioactive particles.


                                              30
Assigning Dose of Record
    Shallow Dose Equivalent
 
    There were no dose assessments for shallow dose equivalent available for review. The
For the special dosimetry situations reviewed in this section, the inspectors assessed how CENG assigns dose of record for total effective dose equivalent, shallow dose equivalent, and lens dose equivalent. This included an assessment of external and  
    inspectors evaluated CENGs method for calculating shallow dose equivalent from
internal monitoring results, supplementa
    distributed skin contamination or discrete radioactive particles.
ry information on individual exposures, and radiation surveys when dose assessment was based on these techniques.  
    Assigning Dose of Record
    For the special dosimetry situations reviewed in this section, the inspectors assessed
    how CENG assigns dose of record for total effective dose equivalent, shallow dose
    equivalent, and lens dose equivalent. This included an assessment of external and
    internal monitoring results, supplementary information on individual exposures, and
    radiation surveys when dose assessment was based on these techniques.
    Problem Identification and Resolution
    The inspectors assessed whether problems associated with occupational dose
    assessment are being identified by CENG at an appropriate threshold and are properly
    being addressed for resolution in CENGs CAP. The inspectors assessed the
    appropriateness of the corrective actions for a selected sample of problems documented
    by CENG involving occupational dose assessment.
b.  Findings
    No findings were identified.
2RS7 Radiological Environmental Monitoring Program (71124.07)
a.  Inspection Scope
    From May 6 to 10, 2013, the inspectors verified that the radiological environmental
    monitoring program (REMP) quantifies the impact of radioactive effluent released to the
    environment and sufficiently validates the integrity of the radioactive gaseous and liquid
    effluent release program.
    The inspectors used the requirements in 10 CFR 20; 10 CFR 50, Appendix A, Criterion
    60, Control of Release of Radioactivity to the Environment; 10 CFR 50, Appendix I,
    Numerical Guides for Design Objectives and Limiting Conditions for Operations to Meet
    the Criterion As Low As Is Reasonably Achievable for Radioactive Material in Light-
    Water-Cooled Nuclear Power Reactor Effluents; 40 CFR 190, Environmental Radiation
    Protection Standards for Nuclear Power Operations; 40 CFR 141, Maximum
    Contaminant Levels for Radionuclides; RG 1.23, Meteorological Monitoring Programs
    for Nuclear Power Plants; RG 4.1, Radiological Environmental Monitoring for Nuclear
    Power Plants; RG 4.15, Quality Assurance for Radiological Monitoring Programs;
    NUREG-1302, Offsite Dose Calculation Manual Guidance: Standard Radiological
    Effluent Controls for Boiling Water Reactors; applicable industry standards; and CENG
    procedures as criteria for determining compliance.
                                                                                      Enclosure


Problem Identification and Resolution
                                        31
 
Inspection Planning
The inspectors assessed whether problems associated with occupational dose  
The inspectors reviewed CENGs annual radiological environmental operating reports for
assessment are being identified by CENG at an appropriate threshold and are properly
2011 and 2012 and the results of any assessments since the last inspection to verify that
being addressed for resolution in CENG's CAP. The inspectors assessed the appropriateness of the corrective actions for a selected sample of problems documented by CENG involving occupational dose assessment.  
the REMP was implemented and reported in accordance with requirements. This review
 
included changes to the offsite dose calculation manual (ODCM) in environmental
  b. Findings
monitoring, sampling locations, monitoring and measurement frequencies, land-use
 
census, inter-laboratory comparison program, and analysis of environmental data.
No findings were identified.  
The inspectors reviewed Units 1 and 2 ODCMs to identify locations of environmental
2RS7 Radiological Environmental Monitoring Program
monitoring stations. The inspectors reviewed Units 1 and 2 UFSARs for information
(71124.07)
regarding the environmental monitoring program and meteorological monitoring
 
instrumentation. The inspectors reviewed quality assurance audits and technical
  a. Inspection Scope
evaluations performed on the vendor analytical laboratory program.
  From May 6 to 10, 2013, the inspectors verified that the radiological environmental
The inspectors reviewed Units 1 and 2 radioactive effluent release reports for 2011 and
monitoring program (REMP) quantifies the impact of radioactive effluent released to the environment and sufficiently validates the integrity of the radioactive gaseous and liquid
2012 and the most recent results from waste stream analysis to determine if CENG was
effluent release program.  
sampling and analyzing for the predominant radionuclides released in plant effluents.
 
Site Environmental Inspection
The inspectors walked down five air sampling stations and five environmental thermo
The inspectors used the requirements in 10 CFR 20; 10 CFR 50, Appendix A, Criterion 60, "Control of Release of Radioactivity to the Environment;" 10 CFR 50, Appendix I, "Numerical Guides for Design Objectives and Limiting Conditions for Operations to Meet
luminescent dosimeter (TLD) monitoring stations to determine whether they were
the Criterion As Low As Is Reasonably Achi
located as described in the ODCM and to determine the equipment material condition.
evable for Radioactive Material in Light-Water-Cooled Nuclear Power Reactor Effluents;" 40 CFR 190, "Environmental Radiation
For the air samplers and TLD stations selected, the inspectors reviewed the calibration
Protection Standards for Nuclear Power Operations;" 40 CFR 141, "Maximum Contaminant Levels for Radionuclides;" RG 1.23, "Meteorological Monitoring Programs for Nuclear Power Plants;" RG 4.1, "Radiological Environmental Monitoring for Nuclear
and maintenance records to verify that they demonstrated adequate operability for these
Power Plants;" RG 4.15, "Quality Assurance for Radiological Monitoring Programs;"
components. Additionally, the review included the calibration and maintenance records
NUREG-1302, "Offsite Dose Calculation Manual Guidance:  Standard Radiological
of four composite water samplers.
Effluent Controls for Boiling Water Reactors;" applicable industry standards; and CENG
The inspectors performed an assessment of any compensatory environmental sampling
procedures as criteria for determining compliance.  
upon loss of a required sampling station.
 
The inspectors observed the collection and preparation of four environmental samples
from surface water and fish to verify that environmental sampling was representative of
 
the effluent release pathways as specified in the ODCM and that sampling techniques
31  Enclosure Inspection Planning
were in accordance with procedures.
 
Based on direct observation and review of records, the inspectors assessed whether the
The inspectors reviewed CENG's annual radiological environmental operating reports for 2011 and 2012 and the results of any assessments since the last inspection to verify that the REMP was implemented and reported in accordance with requirements. This review included changes to the offsite dose calculation manual (ODCM) in environmental
meteorological instruments were operable, calibrated, and maintained in accordance
with procedures. The inspectors assessed whether the meteorological data readout and
recording instruments in the control room and at the meteorological tower were operable
and accurate.
The inspectors evaluated whether missed and/or anomalous environmental samples
were identified and reported in the annual radiological environmental operating reports.
The inspectors selected five events that involved a missed sample or inoperable sampler
to verify that CENG had identified the cause and had implemented corrective actions.
The inspectors reviewed the assessment of any sample results detected above the
lower limits of detection and reviewed CENGs evaluation of associated radioactive
effluent release data that was the potential source of the released material. The 2011
                                                                                Enclosure


monitoring, sampling locations, monitoring and measurement frequencies, land-use census, inter-laboratory comparison program, and analysis of environmental data.
                                          32
 
radiological environmental operator report noted the detection of Iodine from the
The inspectors reviewed Units 1 and 2 ODCMs to identify locations of environmental monitoring stations.  The inspectors reviewed Units 1 and 2 UFSARs for information
Fukushima Daiichi accident during March and April 2011.
regarding the environmental monitoring program and meteorological monitoring
The inspectors selected the following five SSCs that contained licensed material for
instrumentation.  The inspectors reviewed quality assurance audits and technical
which there was a credible mechanism for radioactive material to reach ground water:
evaluations performed on the vendor analytical laboratory program.
  Unit 1 drywell, reactor, and turbine building sumps
The inspectors reviewed Units 1 and 2 radioactive effluent release reports for 2011 and
  Unit 2 drywell, reactor, and turbine building sumps
2012 and the most recent results from waste stream analysis to determine if CENG was
  Unit 2 stack condensate transfer line to radwaste
sampling and analyzing for the predominant radionuclides released in plant effluents.
  Old radwaste sumps W 11, 12, and 13, and concentrator waste tank cubicle
 
  Waste water treatment facility clarified tanks and sludge pits
Site Environmental Inspection
The inspectors assessed whether CENG had implemented a sampling, inspection, and
 
monitoring program to provide early detection of leakage from these SSCs to ground
The inspectors walked down five air sampling stations and five
water.
environmental thermo luminescent dosimeter (TLD) monitoring stations to determine whether they were
The inspectors evaluated whether decommissioning records of leaks, spills, and
located as described in the ODCM and to determine the equipment material condition.
environmental remediation since the previous inspection were retained in a retrievable
 
manner in the 10 CFR 50.75(g) decommissioning file. Two records were added to the
For the air samplers and TLD stations selected, the inspectors reviewed the calibration and maintenance records to verify that they demonstrated adequate operability for these
decommissioning file in 2012. The first was Unit 1 turbine building roof replacement,
 
and the second was tritium in-leakage to the Unit 1 screen house.
components.  Additionally, the review included the calibration and maintenance records of four composite water samplers.
The inspectors reviewed any significant changes made by CENG to the ODCM as the
 
result of changes to the land census, long-term meteorological conditions, or
The inspectors performed an assessment of any compensatory environmental sampling upon loss of a required sampling station.
modifications to the sampler stations since the last inspection. The inspectors reviewed
 
technical justifications for any changed sampling locations to ensure that the changes
did not affect CENGs ability to monitor the impact of plant operations on the
The inspectors observed the collection and preparation of four environmental samples
environment.
from surface water and fish to verify that environmental sampling was representative of
The inspectors assessed whether the detection sensitivities for environmental samples
the effluent release pathways as specified in the ODCM and that sampling techniques were in accordance with procedures.
were below the lower limits of detection specified in the ODCM. The inspectors
reviewed quality control charts for laboratory radiation measurement instrument and
Based on direct observation and review of records, the inspectors assessed whether the
actions taken for degrading detector performance. The inspectors also reviewed the
meteorological instruments were operable, calibrated, and maintained in accordance
results of the vendors quality control program including the inter-laboratory comparison
with procedures.  The inspectors assessed whether the meteorological data readout and recording instruments in the control room and at the meteorological tower were operable and accurate.
to assess the adequacy of the vendors program.
 
The inspectors reviewed the results of Entergy Nuclear Northeast (Entergy) inter-
laboratory and intra-laboratory comparison program to verify the adequacy of
The inspectors evaluated whether missed and/or anomalous environmental samples
environmental sample analyses performed by James A. Fitzpatrick Nuclear Power Plant
were identified and reported in the annual radiological environmental operating reports.  The inspectors selected five events that involved a missed sample or inoperable sampler to verify that CENG had identified the cause and had implemented corrective actions.  The inspectors reviewed the assessment of any sample results detected above the
environmental laboratory. The inspectors assessed whether the results included for the
lower limits of detection and reviewed CENG's evaluation of associated radioactive
media radionuclide mix was appropriate for the facility.
effluent release data that was the potential source of the released material.  The 2011 
32  Enclosure radiological environmental operator report noted the detection of Iodine from the Fukushima Daiichi accident during March and April 2011. The inspectors selected the following five SSCs that contained licensed material for which there was a credible mechanism for radioactive material to reach ground water:  
 
  Unit 1 drywell, reactor, and turbine building sumps Unit 2 drywell, reactor, and turbine building sumps Unit 2 stack condensate transfer line to radwaste Old radwaste sumps W 11, 12, and 13, and concentrator waste tank cubicle Waste water treatment facility clarified tanks and sludge pits  
The inspectors assessed whether CENG had implemented a sampling, inspection, and  
monitoring program to provide early detection of leakage from these SSCs to ground  
 
water.  
The inspectors evaluated whether decommissioning records of leaks, spills, and environmental remediation since the previous inspection were retained in a retrievable manner in the 10 CFR 50.75(g) decommissioning file. Two records were added to the  
decommissioning file in 2012. The first was Unit 1 turbine building roof replacement,  
and the second was tritium in-leakage to the Unit 1 screen house.  
 
The inspectors reviewed any significant changes made by CENG to the ODCM as the result of changes to the land census, long-term meteorological conditions, or  
modifications to the sampler stations since the last inspection. The inspectors reviewed  
technical justifications for any changed sampling locations to ensure that the changes  
did not affect CENG's ability to monitor the impact of plant operations on the  
environment.   The inspectors assessed whether the detection sensitivities for environmental samples were below the lower limits of detection specified in the ODCM. The inspectors  
reviewed quality control charts for laboratory radiation measurement instrument and actions taken for degrading detector performance. The inspectors also reviewed the results of the vendor's quality control program including the inter-laboratory comparison  
to assess the adequacy of the vendor's program.  
 
The inspectors reviewed the results of Entergy Nuclear Northeast (Entergy) inter-laboratory and intra-laboratory comparison program to verify the adequacy of environmental sample analyses performed by James A. Fitzpatrick Nuclear Power Plant  
environmental laboratory. The inspectors assessed whether the results included for the  
media radionuclide mix was appropriate for the facility.  
 
Identification and Resolution of Problems
Identification and Resolution of Problems
  The inspectors assessed whether problems associated with the REMP and  
The inspectors assessed whether problems associated with the REMP and
meteorological monitoring programs were being identified by CENG at an appropriate  
meteorological monitoring programs were being identified by CENG at an appropriate
threshold and correction actions were assigned for resolution in CENG's CAP.  
threshold and correction actions were assigned for resolution in CENGs CAP.
                                                                                Enclosure


   
                                            33
33  Enclosure   b. Findings
   b. Findings
 
    No findings were identified.
No findings were identified.  
4.   OTHER ACTIVITIES
4. OTHER ACTIVITIES
4OA1 Performance Indicator Verification (71151)
  4OA1 Performance Indicator Verification (71151)
    RCS Specific Activity and RCS Leak Rate (4 samples)
RCS Specific Activity and RCS Leak Rate (4 samples)  
  a. Inspection Scope
  The inspectors reviewed CENG's submittal for the RCS specific activity (BI01) and RCS
leak rate (BI02) performance indicators for both Unit 1 and Unit 2 for the period of April 1, 2011, through March 31, 2013.  (Note: An additional 12 months of BI02 data was reviewed due to CENG having updated and revised the BI02 performance indicator data
since the previous inspection.)  To determine the accuracy of the performance indicator
reported during those periods, the inspectors used definitions and guidance contained in
 
Nuclear Energy Institute Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 6.  The inspectors also reviewed RCS sample analysis and control room logs of daily measur
ements of RCS leakage and compared that information to the data reported by the performance indicator.  Additionally, the inspectors observed surveillance activities that determined the RCS identified leakage
rate, and chemistry personnel taking and analyzing an RCS sample.
  b. Findings
 
No findings were identified.
 
4OA2 Problem Identification and Resolution (71152 - 4 samples)
.1 Routine Review of Problem Identification and Resolution Activities
 
   a. Inspection Scope
   a. Inspection Scope
  As required by Inspection Procedure 71152, "Problem Identification and Resolution," the
    The inspectors reviewed CENGs submittal for the RCS specific activity (BI01) and RCS
inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that CENG entered issues into the CAP at an appropriate
    leak rate (BI02) performance indicators for both Unit 1 and Unit 2 for the period of April
threshold, gave adequate attention to timely corrective actions, and identified and  
    1, 2011, through March 31, 2013. (Note: An additional 12 months of BI02 data was
addressed adverse trends. In order to assist with the identification of repetitive
    reviewed due to CENG having updated and revised the BI02 performance indicator data
equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the CAP.  
    since the previous inspection.) To determine the accuracy of the performance indicator
    reported during those periods, the inspectors used definitions and guidance contained in
    Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance
    Indicator Guideline, Revision 6. The inspectors also reviewed RCS sample analysis
    and control room logs of daily measurements of RCS leakage and compared that
    information to the data reported by the performance indicator. Additionally, the
    inspectors observed surveillance activities that determined the RCS identified leakage
    rate, and chemistry personnel taking and analyzing an RCS sample.
   b. Findings
   b. Findings
  No findings were identified.  
    No findings were identified.
 
4OA2 Problem Identification and Resolution (71152 - 4 samples)
.1   Routine Review of Problem Identification and Resolution Activities
    
34  Enclosure .2 Semi-Annual Trend Review
 
   a. Inspection Scope
   a. Inspection Scope
  The inspectors performed a semi-annual review of site issues, as required by Inspection  
    As required by Inspection Procedure 71152, Problem Identification and Resolution, the
Procedure 71152 to identify trends that might indicate the existence of more significant
    inspectors routinely reviewed issues during baseline inspection activities and plant
safety issues.  In this review, the inspectors included repetitive or closely related issues  
    status reviews to verify that CENG entered issues into the CAP at an appropriate
that may have been documented by CENG outside of the CAP such as trend reports,
    threshold, gave adequate attention to timely corrective actions, and identified and
performance indicators, major equipment problem lists, system health reports, maintenance rule assessments, and maintenance or CAP backlogs. The inspectors also reviewed CENG's CAP database for the first and second quarters of 2013 to assess
    addressed adverse trends. In order to assist with the identification of repetitive
condition reports written in various s
    equipment failures and specific human performance issues for follow-up, the inspectors
ubject areas (equipment problems, human performance issues, etc.) as well as indivi
    performed a daily screening of items entered into the CAP.
dual issues identified
  b. Findings
during the NRC's daily condition report review (Section 4OA2.1).  The inspectors reviewed CENG's quarterly trend report for the first quarter of 2013 conducted under CNG-QL-1.01-1008, "Periodic QPA Performance Reporting Process," Revision 00500, to verify that CENG
    No findings were identified.
personnel were appropriately evaluating and trending adverse conditions in accordance with
                                                                                        Enclosure
applicable procedures.


  b. Findings and Observations
                                                34
  No findings were identified.  
.2  Semi-Annual Trend Review
 
  a. Inspection Scope
    The inspectors performed a semi-annual review of site issues, as required by Inspection
Two trends were identified by the inspectors that had not been identified by CENG.  
    Procedure 71152 to identify trends that might indicate the existence of more significant
The inspectors noted a negative trend in the reliability and availability of the emergency core cooling system (ECCS) keep-fill pumps on Unit 2. The low-pressure core spray keep-fill pump 2CLS*P2 failed on January 9, 2013, due to motor overload (CR-2013-
    safety issues. In this review, the inspectors included repetitive or closely related issues
000218). On February 28, the HPCS keep-fill pump suddenly failed (CR-2013-001633).
    that may have been documented by CENG outside of the CAP such as trend reports,
As part of an extent-of-condition review for the low-pressure core spray keep-fill pump  
    performance indicators, major equipment problem lists, system health reports,
failing, operators identified that Division II RHR system keep-fill pump 2RHS*P2 motor had an abnormal noise. On April 12, CENG replaced 2RHS*P2 motor. The ECCS keep-fill pumps are Goulds Pump Model 3196ST with 215T Westinghouse motors rated  
    maintenance rule assessments, and maintenance or CAP backlogs. The inspectors also
for 575 volts. Westinghouse investigations determined that each motor had a turn-to-
    reviewed CENGs CAP database for the first and second quarters of 2013 to assess
turn failure. The failure of the HPCS keep-fill pump resulted in Licensee Event Report  
    condition reports written in various subject areas (equipment problems, human
(LER) 2013-002, "Failure of High-Pressure Core Spray System Pressure Pump due to a  
    performance issues, etc.) as well as individual issues identified during the NRCs daily
 
    condition report review (Section 4OA2.1). The inspectors reviewed CENGs quarterly
Motor Winding Failure," in accordance with 10 CFR Part 50.73(a)(2)(v)(D) and 10 CFR Part 21. All three keep-fill pump motors have been replaced, and CENG has entered these issues into their CAP as noted by the condition reports above.  
    trend report for the first quarter of 2013 conducted under CNG-QL-1.01-1008, Periodic
    QPA Performance Reporting Process, Revision 00500, to verify that CENG personnel
    were appropriately evaluating and trending adverse conditions in accordance with
    applicable procedures.
  b. Findings and Observations
    No findings were identified.
    Two trends were identified by the inspectors that had not been identified by CENG.
    The inspectors noted a negative trend in the reliability and availability of the emergency
    core cooling system (ECCS) keep-fill pumps on Unit 2. The low-pressure core spray
    keep-fill pump 2CLS*P2 failed on January 9, 2013, due to motor overload (CR-2013-
    000218). On February 28, the HPCS keep-fill pump suddenly failed (CR-2013-001633).
    As part of an extent-of-condition review for the low-pressure core spray keep-fill pump
    failing, operators identified that Division II RHR system keep-fill pump 2RHS*P2 motor
    had an abnormal noise. On April 12, CENG replaced 2RHS*P2 motor. The ECCS
    keep-fill pumps are Goulds Pump Model 3196ST with 215T Westinghouse motors rated
    for 575 volts. Westinghouse investigations determined that each motor had a turn-to-
    turn failure. The failure of the HPCS keep-fill pump resulted in Licensee Event Report
    (LER) 2013-002, Failure of High-Pressure Core Spray System Pressure Pump due to a
    Motor Winding Failure, in accordance with 10 CFR Part 50.73(a)(2)(v)(D) and 10 CFR
    Part 21. All three keep-fill pump motors have been replaced, and CENG has entered
    these issues into their CAP as noted by the condition reports above.
    The inspectors noted a decrease in the reliability of the Unit 1 RB sumps, and as a
    result, an increase in the number of emergency operating procedure entries by control
    room operators due to sump failures. The decrease in reliability was noted by three
    separate events regarding Unit 1 RB sumps that resulted in emergency operating
    procedure entries. These events occurred on January 20, April 12, and April 24, and
    were documented in CR-2013-000532, CR-2013-002743 and CR-2013-003371,
    respectively. The inspectors review identified that although CENG had properly
    assessed sump performance per the NRC maintenance rule 10 CFR 50.65 for the train
    level criteria, CENG did not assess sump performance against the system level criteria.
    CENG documented this issue in CR-2013-004828 and entered this issue into their CAP.
    A subsequent CENG evaluation determined the RB floor and equipment sumps had
    exceeded their performance monitoring group functional failure criteria and the systems
                                                                                        Enclosure


                                              35
The inspectors noted a decrease in the reliability of the Unit 1 RB sumps, and as a
    were placed into (a)(1) status. The inspectors determined that this issue was not more
result, an increase in the number of emergency operating procedure entries by control room operators due to sump failures.  The decrease in reliability was noted by three separate events regarding Unit 1 RB sumps that resulted in emergency operating
    than minor because the train level criteria were appropriately being monitored and
procedure entries.  These events occurred on January 20, April 12, and April 24, and
    placing the RB sumps into (a)(1) status for exceeding system level criteria would not
were documented in CR-2013-000532, CR-2013-002743 and CR-2013-003371,
    have resulted in additional maintenance-related corrective actions being taken by
respectively.  The inspector's review identified that although CENG had properly
    CENG.
assessed sump performance per the NRC maintenance rule 10 CFR 50.65 for the train level criteria, CENG did not assess sump performance against the system level criteria.  CENG documented this issue in CR-2013-004828 and entered this issue into their CAP. 
.3   Annual Sample: Review of Repetitive Valve Packing Leakage Issues
A subsequent CENG evaluation determined the RB floor and equipment sumps had
 
exceeded their performance monitoring group functional failure criteria and the systems 
35  Enclosure were placed into (a)(1) status. The inspectors determined that this issue was not more than minor because the train level criteria were appropriately being monitored and  
placing the RB sumps into (a)(1) status for exceeding system level criteria would not have resulted in additional maintenance-related corrective actions being taken by  
CENG.  
.3 Annual Sample: Review of Repetitive Valve Packing Leakage Issues
 
   a. Inspection Scope
   a. Inspection Scope
  The inspectors performed an in-depth review of CENG's root cause analysis and  
    The inspectors performed an in-depth review of CENGs root cause analysis and
corrective actions associated with CR-2011-007171 and CR-2011-010906 regarding two  
    corrective actions associated with CR-2011-007171 and CR-2011-010906 regarding two
forced shutdowns of Unit 2 due to excessive unidentified leak rates in 2011. The  
    forced shutdowns of Unit 2 due to excessive unidentified leak rates in 2011. The
inspectors focused on the implementation of corrective actions and extent-of-condition and cause reviews as it applied to both units.  
    inspectors focused on the implementation of corrective actions and extent-of-condition
    and cause reviews as it applied to both units.
The inspectors assessed CENG's problem identification threshold, cause analyses,  
    The inspectors assessed CENGs problem identification threshold, cause analyses,
extent-of-condition reviews, compensatory actions, and the prioritization and timeliness  
    extent-of-condition reviews, compensatory actions, and the prioritization and timeliness
of CENG's corrective actions to determine whether CENG was appropriately identifying, characterizing, and correcting problems associated with this issue and whether the planned or completed corrective actions were appropriate. The inspectors compared the  
    of CENGs corrective actions to determine whether CENG was appropriately identifying,
actions taken to the requirements of CENG's CAP and 10 CFR 50, Appendix B. In  
    characterizing, and correcting problems associated with this issue and whether the
addition, the inspectors performed field walkdowns and interviewed engineering  
    planned or completed corrective actions were appropriate. The inspectors compared the
personnel to assess the effectiveness of the implemented corrective actions.   
    actions taken to the requirements of CENGs CAP and 10 CFR 50, Appendix B. In
  b. Findings and Observations
    addition, the inspectors performed field walkdowns and interviewed engineering
  No findings were identified.  
    personnel to assess the effectiveness of the implemented corrective actions.
On August 6 and December 9, 2011, Unit 2 conducted forced shutdowns due to excessive unidentified leakage rate. In both cases, the increased unidentified leakage was determined to be from the failure of the recirculation discharge gate valve,  
   b. Findings and Observations
2RCS*MOV18A. CENG completed separate root cause analysis for both events and  
    No findings were identified.
determined the August 6 event was due to a design issue which subjects the packing to  
    On August 6 and December 9, 2011, Unit 2 conducted forced shutdowns due to
excessive vibrations due to the valve gate being exposed to RCS system flow. The  
    excessive unidentified leakage rate. In both cases, the increased unidentified leakage
December 9 event was determined to be the result of a workmanship error following the August 6 event which resulted in a burr forming on the valve stem and eventually led to the second packing failure.  
    was determined to be from the failure of the recirculation discharge gate valve,
 
    2RCS*MOV18A. CENG completed separate root cause analysis for both events and
    determined the August 6 event was due to a design issue which subjects the packing to
The inspectors reviewed the root cause analysis and the ECP associated with the 2001  
    excessive vibrations due to the valve gate being exposed to RCS system flow. The
change in packing design for this valve. The inspectors reviewed photos and drawings of the valve and interviewed engineering personnel. The inspectors concluded that CENGs determination of the root cause and major contributing causes were reasonable  
    December 9 event was determined to be the result of a workmanship error following the
and had a sound technical basis. The inspectors also determined that corrective actions  
    August 6 event which resulted in a burr forming on the valve stem and eventually led to
 
    the second packing failure.
for the August 6 event would not have been expected to preclude the December 9 event.  
    The inspectors reviewed the root cause analysis and the ECP associated with the 2001
    change in packing design for this valve. The inspectors reviewed photos and drawings
The inspectors reviewed CENG's extent-of-condition reviews and corrective actions related to similar valves on both Units 1 and 2. The inspectors concluded that CENG conducted an appropriate extent-of-condition review and identified other valves which
    of the valve and interviewed engineering personnel. The inspectors concluded that
 
    CENGs determination of the root cause and major contributing causes were reasonable
    and had a sound technical basis. The inspectors also determined that corrective actions
 
    for the August 6 event would not have been expected to preclude the December 9 event.
36  Enclosure may be susceptible to the same failure mechanism.  CENG also developed corrective actions to enhance their valve packing program and designated an engineer to oversee
    The inspectors reviewed CENGs extent-of-condition reviews and corrective actions
 
    related to similar valves on both Units 1 and 2. The inspectors concluded that CENG
this program.
    conducted an appropriate extent-of-condition review and identified other valves which
The inspectors conducted an independent review of condition reports from 2000 until the
                                                                                      Enclosure
present looking for excessive leakage issues associated with valve packing.  The
inspectors confirmed that a large percentage of issues prior to 2001 and since 2007
have been related to RCS*MOV18A and the underlying design vulnerability.  Corrective
actions related to this issue included enhancing torque specification values for the packing, developing preventive maintenance items to re-torque the packing periodically, and revising work packages.  The inspectors determined these corrective actions were
reasonable and had been implemented appropriately and in a timely manner.


                                                36
The inspectors also observed that appropriate effectiveness reviews were either completed or were scheduled to be completed in a timely manner.  
    may be susceptible to the same failure mechanism. CENG also developed corrective
    actions to enhance their valve packing program and designated an engineer to oversee
.4 Annual Sample: Human Performance Safety Culture Themes  
    this program.
 
    The inspectors conducted an independent review of condition reports from 2000 until the
    present looking for excessive leakage issues associated with valve packing. The
    inspectors confirmed that a large percentage of issues prior to 2001 and since 2007
    have been related to RCS*MOV18A and the underlying design vulnerability. Corrective
    actions related to this issue included enhancing torque specification values for the
    packing, developing preventive maintenance items to re-torque the packing periodically,
    and revising work packages. The inspectors determined these corrective actions were
    reasonable and had been implemented appropriately and in a timely manner.
    The inspectors also observed that appropriate effectiveness reviews were either
    completed or were scheduled to be completed in a timely manner.
.4   Annual Sample: Human Performance Safety Culture Themes
   a. Inspection Scope
   a. Inspection Scope
  This inspection focused on CENGs' evaluation and resolution of an emerging theme in  
    This inspection focused on CENGs evaluation and resolution of an emerging theme in
the number of human performance cross-cutting issues associated with NRC inspection findings. Specifically, in the third quart
    the number of human performance cross-cutting issues associated with NRC inspection
er of 2012, four NRC Green inspection findings across multiple cornerstones were identified as having common cross-cutting aspects in  
    findings. Specifically, in the third quarter of 2012, four NRC Green inspection findings
the area of Human Performance, Resources, [H.2(c)], because CENG did not provide complete, accurate, and up-to-date procedures that were adequate to assure nuclear safety. On August 9, 2012, CENG initiated CR-2012-007529 and performed an  
    across multiple cornerstones were identified as having common cross-cutting aspects in
apparent cause evaluation to assess this trend. The NRC completed Inspection  
    the area of Human Performance, Resources, [H.2(c)], because CENG did not provide
Procedure 71152 in the form of a problem identification and resolution annual sample to  
    complete, accurate, and up-to-date procedures that were adequate to assure nuclear
assess this trend during the fourth quarter of 2012 to provide information to support the end of cycle assessment. Subsequently, on November 7, CENG initiated CR-2012-010211, "A Cross-Cutting Theme Exists in the Aspect of Human Performance,  
    safety. On August 9, 2012, CENG initiated CR-2012-007529 and performed an
Resources, Documentation [H.2(c)]," to further assess and address this adverse trend.
    apparent cause evaluation to assess this trend. The NRC completed Inspection
A root cause analysis was completed and corrective actions were recommended for  
    Procedure 71152 in the form of a problem identification and resolution annual sample to
implementation. The inspectors selected this emerging trend for further review to  
    assess this trend during the fourth quarter of 2012 to provide information to support the
develop more recent insights into CENG's progress in addressing the cross-cutting theme to provide meaningful input to the mid-cycle assessment process. The inspectors reviewed CENG condition reports, the root cause evaluation, and corrective, preventive, and compensatory actions associated with the emerging theme. The inspectors also  
    end of cycle assessment. Subsequently, on November 7, CENG initiated CR-2012-
interviewed plant personnel. The four findings associated with cross-cutting theme  
    010211, A Cross-Cutting Theme Exists in the Aspect of Human Performance,
H.2(c) are summarized as follows:  
    Resources, Documentation [H.2(c)], to further assess and address this adverse trend.
  Unit 1 - Inadequate torque applied to SDC isolation valve closure bolts (CR-2012-
    A root cause analysis was completed and corrective actions were recommended for
001441) Unit 2 - Loss of SFP cooling due an inadequate procedure (CR-2012-004850) Unit 2 - Inadequate special operating procedure for loss of SFP cooling (CR-2012-
    implementation. The inspectors selected this emerging trend for further review to
007811) Unit 2 - Inadequate evaluation and implementation of design modification to the turbine gland seal supply system (CR-2012-006615)  
    develop more recent insights into CENGs progress in addressing the cross-cutting
 
    theme to provide meaningful input to the mid-cycle assessment process. The inspectors
37  Enclosure   b. Findings and Observations
    reviewed CENG condition reports, the root cause evaluation, and corrective, preventive,
  No findings were identified. 
    and compensatory actions associated with the emerging theme. The inspectors also
CENG identified an adverse trend existed in the cross-cutting aspect H.2(c) and
    interviewed plant personnel. The four findings associated with cross-cutting theme
recognized that the theme affected broad areas of performance as assessed in the
    H.2(c) are summarized as follows:
fourth quarter of 2012.  CENG completed the root cause assessment for the adverse
        Unit 1 - Inadequate torque applied to SDC isolation valve closure bolts (CR-2012-
trend in the H.2(c) cross-cutting aspect in December 2012.  The root cause analysis
        001441)
evaluated the four Green findings and also independently determined the common causes of these findings. 
        Unit 2 - Loss of SFP cooling due an inadequate procedure (CR-2012-004850)
        Unit 2 - Inadequate special operating procedure for loss of SFP cooling (CR-2012-
CENG concluded that the work and administrative control documents and processes
        007811)
were adequate, but the implementation of these processes was not adequate.  Formal
        Unit 2 - Inadequate evaluation and implementation of design modification to the
techniques were used to reach this conclusion.  The 46 specific causal factors from the four findings were generalized into 13 general causal areas which were further condensed (or binned) into five causal themes.  The process of generalization of the
        turbine gland seal supply system (CR-2012-006615)
causal factors resulted in the majority of causal factors (53 percent) having the theme of
                                                                                      Enclosure
"lack of engineering /challenge assumptions /mindset (willingness to accept answer with
no challenge)."  CENG further concluded "a less rigorous standard resulted in products that were of insufficient quality.  The error drivers may be both process and behavior; however, the results of the common cause analyses did not indicate that process
problems were significant errors." 
 
CENG determined that the root cause of the trend was that site leadership had not
identified marginal performance relative to the technical rigor in the production of work execution documents and, as such, has not put in place corresponding corrective or mitigating strategies.  A contributing cause was listed that existing administrative
controls governing changes to work orders and reviews of said changes are too lenient


to ensure high quality documents are consistently prepared to support plant operations and maintenance activities.  
                                            37
The root cause team recommended 22 corrective actions in the report. CENG  
b. Findings and Observations
management translated these recommendations into 20 unique corrective actions to be  
  No findings were identified.
implemented, 18 of which had been completed by the end of the first quarter 2013. The  
  CENG identified an adverse trend existed in the cross-cutting aspect H.2(c) and
two remaining corrective actions were to complete quarterly effectiveness reviews and a  
  recognized that the theme affected broad areas of performance as assessed in the
final effectiveness review. The assigned corrective action to prevent recurrence (CAPR159) was formulated to develop and communicate a station policy addressing work documentation quality.  
  fourth quarter of 2012. CENG completed the root cause assessment for the adverse
  trend in the H.2(c) cross-cutting aspect in December 2012. The root cause analysis
  evaluated the four Green findings and also independently determined the common
  causes of these findings.
  CENG concluded that the work and administrative control documents and processes
  were adequate, but the implementation of these processes was not adequate. Formal
  techniques were used to reach this conclusion. The 46 specific causal factors from the
  four findings were generalized into 13 general causal areas which were further
  condensed (or binned) into five causal themes. The process of generalization of the
  causal factors resulted in the majority of causal factors (53 percent) having the theme of
  lack of engineering /challenge assumptions /mindset (willingness to accept answer with
  no challenge). CENG further concluded a less rigorous standard resulted in products
  that were of insufficient quality. The error drivers may be both process and behavior;
  however, the results of the common cause analyses did not indicate that process
  problems were significant errors.
  CENG determined that the root cause of the trend was that site leadership had not
  identified marginal performance relative to the technical rigor in the production of work
  execution documents and, as such, has not put in place corresponding corrective or
  mitigating strategies. A contributing cause was listed that existing administrative
  controls governing changes to work orders and reviews of said changes are too lenient
  to ensure high quality documents are consistently prepared to support plant operations
  and maintenance activities.
  The root cause team recommended 22 corrective actions in the report. CENG
  management translated these recommendations into 20 unique corrective actions to be
  implemented, 18 of which had been completed by the end of the first quarter 2013. The
  two remaining corrective actions were to complete quarterly effectiveness reviews and a
  final effectiveness review. The assigned corrective action to prevent recurrence
  (CAPR159) was formulated to develop and communicate a station policy addressing
  work documentation quality.
  The corrective actions focused substantially on training plant personnel to properly
  implement their procedures and to hold them accountable if they did not follow the
  procedures. Three of the recommended corrective actions involved development of or
  changes to work procedures. CA #59 was to define the term skill of the craft in a
  procedure and was completed on June 12, using guidance obtained from an industry
  group; CA #55 was to develop and implement a fleet conduct of engineering
  administrative procedure and was closed to CA #244 to reinforce current expectations
  for engineering roles and responsibilities; and CA #64 was to develop a process tool to
  assist in screening pen and ink changes to procedures. This corrective action was also
  changed to revise site procedures to add a requirement to initiate a condition report if a
  procedure could not be completed as written. All but one corrective action relied on
  knowledge-based corrective actions. The only rule-based corrective action was CA #59.
                                                                                    Enclosure


                                                38
The corrective actions focused substantially on training plant personnel to properly
    Although the majority of the corrective actions were knowledge-based activities that
implement their procedures and to hold them accountable if they did not follow the procedures.  Three of the recommended corrective actions involved development of or changes to work procedures.  CA #59 was to define the term "skill of the craft" in a
    relied upon one-time training presentations, only two corrective actions were
procedure and was completed on June 12, using guidance obtained from an industry
    implemented to conduct a needs analysis for the specified training. The needs analysis
group; CA #55 was to develop and implement a fleet conduct of engineering
    for CA #58 (improve the use of SDS-006 for bolt-torque requirements) and CA #164
administrative procedure and was closed to CA #244 to reinforce current expectations
    (understanding the work order process) both concluded that no additional or recurring
for engineering roles and responsibilities; and CA #64 was to develop a process tool to assist in screening pen and ink changes to procedures.  This corrective action was also changed to revise site procedures to add a requirement to initiate a condition report if a
    training were required. The one-time training that had been administered would be
procedure could not be completed as written.  All but one corrective action relied on
    sufficient to correct the adverse trend. As a result, no changes to the initial site training
knowledge-based corrective actions.  The only rule-based corrective action was CA #59.   
    program will be made and these training topics will not be refreshed periodically during
38 Enclosure
    proficiency training.
Although the majority of the corrective actions were knowledge-based activities that  
    The inspectors noted the implemented corrective actions rely almost entirely upon a
relied upon one-time training presentations, only two corrective actions were implemented to conduct a needs analysis for the specified training. The needs analysis for CA #58 (improve the use of SDS-006 for bolt-torque requirements) and CA #164  
    series of one-time training activities to result in institutionalized changes to personnel
(understanding the work order process) both concluded that no additional or recurring  
    behavior and organizational culture into the future. Therefore, the effectiveness of the
training were required. The one-time training that had been administered would be  
    corrective actions could diminish over time as personnel turnover occurs.
sufficient to correct the adverse trend. As a result, no changes to the initial site training  
    The effectiveness reviews for the corrective actions are scheduled to start in the third
program will be made and these training topics will not be refreshed periodically during proficiency training.  
    quarter of 2013. There have been no effectiveness reviews completed on the efficacy of
    the corrective actions for this cross-cutting aspect theme as of June 2013.
The inspectors noted the implemented corrective actions rely almost entirely upon a  
    The inspectors could not conclude that CENGs root cause analysis and resultant
series of one-time training activities to result in institutionalized changes to personnel  
    corrective actions are correct and effective since they have only recently been fully
behavior and organizational culture into the future. Therefore, the effectiveness of the corrective actions could diminish over time as personnel turnover occurs.  
    implemented. However, the number of findings with a cross-cutting aspect in procedure
    adequacy has declined from four to two from the end of cycle to mid cycle NRC reviews.
The effectiveness reviews for the corrective actions are scheduled to start in the third  
.5   Annual Sample: Battery Low Specific Gravities
 
quarter of 2013. There have been no effectiveness reviews completed on the efficacy of  
the corrective actions for this cross-cutting aspect theme as of June 2013.  
The inspectors could not conclude that CENG's root cause analysis and resultant  
corrective actions are correct and effective since they have only recently been fully implemented. However, the number of findings with a cross-cutting aspect in procedure  
adequacy has declined from four to two from the end of cycle to mid cycle NRC reviews.  
.5 Annual Sample: Battery Low Specific Gravities  
 
   a. Inspection Scope
   a. Inspection Scope
  The inspectors performed an in-depth review of CENG's evaluations and corrective actions associated with low-specific gravity in the safety-related station batteries.
    The inspectors performed an in-depth review of CENGs evaluations and corrective
Specifically, an adverse trend of low-specific gravity readings for cells in all three safety-related 125 volts direct current (VDC) station batteries at Unit 2 were identified in  
    actions associated with low-specific gravity in the safety-related station batteries.
CR-2012-001315.   
    Specifically, an adverse trend of low-specific gravity readings for cells in all three
    safety-related 125 volts direct current (VDC) station batteries at Unit 2 were identified in
    CR-2012-001315.
    The inspectors assessed CENGs problem identification threshold, extent-of-condition
    reviews, compensatory actions, and the prioritization and timeliness of CENGs
    corrective actions to determine whether CENG was appropriately identifying,
    characterizing, and correcting problems associated with this issue and whether the
    planned and completed corrective actions were appropriate. The inspectors compared
    the actions taken to the requirements of 10 CFR 50, Appendix B. In addition, the
    inspectors performed field walkdowns and interviewed engineering personnel to assess
    the effectiveness of the implemented corrective actions.
   b. Findings and Observations
    CENG determined the most probable cause of the low-specific gravities was that the
    battery vendors had removed some electrolyte prior to shipping the battery cells to
    NMPNS; and then once at NMPNS, water was added to the cells that diluted the
    concentration of sulfuric acid.
                                                                                          Enclosure


                                              39
The inspectors assessed CENG's problem identification threshold, extent-of-condition reviews, compensatory actions, and the prioritization and timeliness of CENG's corrective actions to determine whether CENG was appropriately identifying,  
    CENG performed a thorough review of the low-specific gravity issue and obtained
characterizing, and correcting problems associated with this issue and whether the  
    information from the battery vendors to support the probable cause. Corrective actions
planned and completed corrective actions were appropriate. The inspectors compared
    included adjusting the method for calculating specific gravity and evaluating adding
the actions taken to the requirements of 10 CFR 50, Appendix B. In addition, the inspectors performed field walkdowns and interviewed engineering personnel to assess the effectiveness of the implemented corrective actions.  
    electrolyte to restore the specific gravity to the manufacturers recommended level.
    CENG verified, based on surveillance testing, that although the specific gravities were
    lower than normal, the concentration of sulfuric acid was adequate to obtain sufficient
    battery capacity to meet the design basis requirements of the batteries.
    The inspectors reviewed condition reports, selected battery test results, and
    correspondence from the battery vendors regarding the low-specific gravity issue. The
    inspectors determined CENGs overall response to the issue was commensurate with
    the safety significance, was timely and included appropriate compensatory actions. The
    inspectors determined that the actions taken were reasonable to resolve the low-specific
    gravity issue. As part of the review, the inspectors determined that two findings existed
    as described below.
b.1 Inadequate Procedural Implementation for Battery Cell Replacement
    Introduction. The inspectors identified a Green NCV of 10 CFR 50, Appendix B,
    Criterion V, Instructions, Procedures, and Drawings, because CENG did not assure
    that the replacement of cells in battery 2C was prescribed and performed by appropriate
    procedures which resulted in degraded accuracy of test results and potential degradation
    to safety-related battery cells.
    Description. The Division III emergency battery bank, battery 2C, at Unit 2 uses jars that
    contain three cells each to provide reliable direct current (DC) power for essential DC
    loads required during normal and abnormal conditions. CENG determined that two jars
    required replacing (a total of six cells). In preparation for this activity, CENG procured
    three jars and stored them in the warehouse. The inspectors determined that several
    procedural inadequacies existed during storage and subsequent cell replacement.
    The cells in the warehouse were not monitored or maintained in accordance with vendor
    recommendations. Specifically, the vendor requires that cells stored in spaces that are
    not air conditioned should have individual cell voltages checked monthly and charged
    when needed to prevent excessive discharge. Although CENG had previously noted
    their poor practices with regards to battery storage and has ongoing corrective actions to
    provide better storage facilities (as documented in CR-2010-012200), CENG did not take
    action to adequately monitor cells in the warehouse. As a result, when the three jars for
    battery 2C were obtained from the warehouse, one was found to be visibly sulfated and
    had to be discarded, and the other two were found undercharged. Sulfation is an
    indication of chronic undercharging and eventually results in permanent loss of capacity.
    Although CR-2012-010907 identified the poor condition of the cells, the cell replacement
    was continued with potentially degraded cells.
    The newly installed cells were not charged prior to or upon installation. This is required
    in the vendor manual and the station battery cell replacement procedure, N2-EMP-GEN-
    673, 24/48 VDC and 125 VDC Batteries - Cell and Connector Replacement, Revision
    00400.
    Battery 2C was then subjected to a modified performance test with the newly installed
    and uncharged cells. This resulted in over-discharging the new cells. Of the new cells,
                                                                                        Enclosure


  b. Findings and Observations
                                            40
  CENG determined the most probable cause of the low-specific gravities was that the battery vendors had removed some electrolyte prior to shipping the battery cells to NMPNS; and then once at NMPNS, water was added to the cells that diluted the  
the two lowest reached 0.903 VDC and 1.167 VDC as opposed to the expected end
concentration of sulfuric acid.  
voltage of approximately 1.75 VDC. This resulted in a battery capacity of 95 percent. In
comparison a normal battery at the age of battery 2C would have a capacity of
approximately 105 percent. Using uncharged cells artificially lowered the test results
which diminished the ability to use the test results for future trending and could mask
poor performance of the remaining cells.
Finally, after the modified performance test, one of the new cells did not recharge
properly. Specifically the vendor states that an equalization charge should be performed
until the lowest cell is within 0.05 volt of the average of all of the cells. During the
equalization charge for battery 2C after the modified performance test, one of the new
cells did not rise to within 0.05 volt of the average of all of the cells. Although CR-2012-
010901 recognized that the acceptance criteria had not been met, the acceptance
criteria was determined to be unnecessary. CENG did not recognize that the failure to
recharge properly was an indication that the previous procedural inadequacies may have
degraded the cell.
CENG entered these inspector-identified issues into the CAP as CR-2013-005235.
CENG corrective actions included reviewing the previous battery 2C test results and the
work order for the next scheduled modified performance test and verifying battery 2C will
remain operable until the next test scheduled for September 2013. CENG also initiated
CR-2013-005074 to replace the two newly installed jars.
Analysis. The inspectors determined that the failure to assure that the replacement of
cells in battery 2C was prescribed and performed by appropriate procedures was a
performance deficiency that was reasonably within CENGs ability to foresee and correct
and should have been prevented. This finding was more than minor because it was
associated with the equipment performance attribute of the Mitigating Systems
cornerstone and affected the cornerstone objective of ensuring the availability, reliability,
and capability of systems that respond to initiating events to prevent undesirable
consequences.
In accordance with IMC 0609.04, Initial Characterization of Findings, and Exhibit 2 of
IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power,
issued June 19, 2012, the inspectors determined this finding to be of very low safety
significance (Green) because the performance deficiency was not a design or
qualification deficiency, did not involve an actual loss of safety function, did not represent
actual loss of a safety function of a single train for greater than its TS allowed outage
time, and did not screen as potentially risk significant due to a seismic, flooding, or
severe weather-initiating event.
This finding has a cross-cutting aspect in the area of Human Performance, Decision-
Making Component, because CENG did not use conservative assumptions in decision
making. Specifically, CENG did not monitor the cells in storage, question the adequacy
of the discharged cells, charge the cells prior to installation, or fully evaluate the
implications of the test and recharge results [H.1(b)].
Enforcement. 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and
Drawings, requires, in part, that activities affecting quality shall be prescribed by
documented instructions, procedures, or drawings of a type appropriate to the
circumstances and shall be accomplished in accordance with these instructions,
                                                                                      Enclosure


 
                                              41
39  Enclosure CENG performed a thorough review of the low-specific gravity issue and obtained information from the battery vendors to support the probable cause. Corrective actions included adjusting the method for calculating specific gravity and evaluating adding electrolyte to restore the specific gravity to the manufacturer's recommended level. CENG verified, based on surveillance testing, that although the specific gravities were
    procedures, or drawings. Contrary to the above, CENG did not assure that the
lower than normal, the concentration of sulfuric acid was adequate to obtain sufficient
    November 2012 replacement of cells in battery 2C was prescribed and performed by
battery capacity to meet the design basis requirements of the batteries.  
    appropriate procedures which resulted in degraded accuracy of test results and potential
    degradation to safety-related battery cells. Because this violation was of very low safety
    significance (Green) and has been entered into CENGs CAP (CR-2013-005235), this
    violation is being treated as an NCV, consistent with Section 2.3.2 of the NRC
    Enforcement Policy. (NCV 05000410/2013003-02, Inadequate Procedural
    Implementation for Battery Cell Replacement)
b.2 Inadequate Design Control for Battery 2C
    Introduction. The inspectors identified a Green NCV of 10 CFR Part 50, Appendix B,
    Criterion III, Design Control, because CENG did not verify the adequacy of the design
    with respect to battery 2C. Specifically, by failing to size the battery to the most limiting
    time period, the sizing calculation significantly overstated the available design margin.
    Description. The Division III emergency battery bank, battery 2C, uses jars that contain
    three cells each to provide reliable DC power for essential DC loads required during
    normal and abnormal conditions at Unit 2. The inspectors reviewed EC-145,
    Verification of Adequacy of Division III Battery 2BYS*BAT2C, Revision 2, to determine
    if the calculation appropriately verified the adequacy of the size of the installed battery
    2C. The inspectors noted that the calculation evaluated the battery based on two time
    periods, a 1-minute period and a 119-minute period. In accordance with Institute of
    Electrical and Electronics Engineers (IEEE) Standard 485-1997, IEEE Recommended
    Practice for Sizing Lead-Acid Batteries for Stationary Applications, and EC-145, the
    battery should be sized based upon the most demanding time period. The inspectors
    determined that the sizing was incorrect. Specifically, although EC-145 determined that
    the first time period (1 minute) was the most demanding, the battery sizing was based
    upon the less demanding second time period (119 minutes).
    In response to this issue, CENG agreed that the calculation was incorrect, entered this
    issue into their CAP (CR-2013-005117), and evaluated the condition for operability.
    CENG performed the battery sizing calculation based upon the correct time period and
    determined that the battery capacity margin reduced from 26 percent to negative
    11 percent (i.e., the battery was undersized by 11 percent). CENG reduced the battery
    design and aging margins from the calculation and were able to increase the capacity
    margin to positive 10 percent which demonstrated a reasonable expectation of
    operability. The significance of reducing the design margin was that the original
    calculation would have permitted modifications to the Division III DC system that could
    have actually overloaded the battery. The significance of reducing the aging margin is
    that the battery would not have been able to perform its design function as the battery
    aged.
    The inspectors independently performed battery sizing calculations and agreed with
    CENGs results.
    Analysis. The inspectors determined that the failure to verify the adequacy of the design
    with respect to battery 2C was a performance deficiency that was reasonably within
    CENGs ability to foresee and correct and should have been prevented. This finding was
    more than minor because it was associated with the design control attribute of the
                                                                                        Enclosure


                                                  42
The inspectors reviewed condition reports, selected battery test results, and correspondence from the battery vendors regarding the low-specific gravity issue.  The inspectors determined CENG's overall response to the issue was commensurate with
    Mitigating Systems cornerstone and affected the cornerstone objective of ensuring the
the safety significance, was timely and included appropriate compensatory actions.  The
    availability, reliability, and capability of systems that respond to initiating events to
inspectors determined that the actions taken were reasonable to resolve the low-specific
    prevent undesirable consequences.
gravity issue.  As part of the review, the inspectors determined that two findings existed as described below.
    In accordance with IMC 0609.04, Initial Characterization of Findings, and Exhibit 2 of
  b.1 Inadequate Procedural Implementation for Battery Cell Replacement
    IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power,
  Introduction.  The inspectors identified a Green NCV of 10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," because CENG did not assure that the replacement of cells in battery 2C was prescribed and performed by appropriate procedures which resulted in degraded accuracy of test results and potential degradation
    issued June 19, 2012, the inspectors determined this finding is of very low safety
to safety-related battery cells.
    significance (Green) because the performance deficiency was not a design or
 
    qualification deficiency, did not involve an actual loss of safety function, did not represent
    actual loss of a safety function of a single train for greater than its TS allowed outage
Description.  The Division III emergency battery bank, battery 2C, at Unit 2 uses jars that contain three cells each to provide reliable direct current (DC) power for essential DC loads required during normal and abnormal conditions.  CENG determined that two jars
    time, and did not screen as potentially risk-significant due to a seismic, flooding, or
required replacing (a total of six cells).  In preparation for this activity, CENG procured three jars and stored them in the warehouse.  The inspectors determined that several
    severe weather-initiating event.
procedural inadequacies existed during storage and subsequent cell replacement.
    This finding did not have a cross-cutting aspect because it was not indicative of current
The cells in the warehouse were not monitored or maintained in accordance with vendor
    performance. Specifically, EC-145 was last revised in 2008.
recommendations.  Specifically, the vendor requires that cells stored in spaces that are
    Enforcement. 10 CFR 50, Appendix B, Criterion III, Design Control, states, in part, that
 
    design control measures shall provide for verifying or checking the adequacy of design.
not air conditioned should have individual cell voltages checked monthly and charged
    Contrary to the above, from July 17, 2008, to June 12, 2013, CENGs design control
when needed to prevent excessive discharge.  Although CENG had previously noted their poor practices with regards to battery storage and has ongoing corrective actions to provide better storage facilities (as documented in CR-2010-012200), CENG did not take action to adequately monitor cells in the warehouse.  As a result, when the three jars for
    measures had not appropriately verified the adequacy of the design regarding battery
battery 2C were obtained from the warehouse, one was found to be visibly sulfated and
    2C. Specifically, by failing to size the battery to the most limiting time period, the sizing
had to be discarded, and the other two were found undercharged.  Sulfation is an
    calculation significantly overstated the available design margin. Because this violation
indication of chronic undercharging and eventually results in permanent loss of capacity.  Although CR-2012-010907 identified the poor condition of the cells, the cell replacement was continued with potentially degraded cells.
    was of very low safety significance (Green) and has been entered into CENGs CAP
 
    (CR-2013-005117), this violation is being treated as an NCV, consistent with Section
    2.3.2 of the NRC Enforcement Policy. (NCV 05000410/2013003-03, Inadequate
The newly installed cells were not charged prior to or upon installation.  This is required
    Design Control for Battery Sizing Calculation)
in the vendor manual and the station battery cell replacement procedure, N2-EMP-GEN-673, "24/48 VDC and 125 VDC Batteries - Cell and Connector Replacement," Revision
4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153 - 6 samples)
00400.   
.1   Plant Events
Battery 2C was then subjected to a modified performance test with the newly installed
and uncharged cells.  This resulted in over-discharging the new cells.  Of the new cells, 
40  Enclosure the two lowest reached 0.903 VDC and 1.167 VDC as opposed to the expected end voltage of approximately 1.75 VDC.  This resulted in a battery capacity of 95 percent.  In
 
comparison a normal battery at the age of battery 2C would have a capacity of approximately 105 percent.  Using uncharged cells artificially lowered the test results which diminished the ability to use the test results for future trending and could  mask
poor performance of the remaining cells.
 
Finally, after the modified performance test, one of the new cells did not recharge
properly.  Specifically the vendor states that an equalization charge should be performed until the lowest cell is within 0.05 volt of the average of all of the cells.  During the equalization charge for battery 2C after the modified performance test, one of the new
cells did not rise to within 0.05 volt of the average of all of the cells.  Although CR-2012-
010901 recognized that the acceptance criteria had not been met, the acceptance
criteria was determined to be unnecessary.  CENG did not recognize that the failure to recharge properly was an indication that the previous procedural inadequacies may have degraded the cell.
 
CENG entered these inspector-identified issues into the CAP as CR-2013-005235.
CENG corrective actions included reviewing the previous battery 2C test results and the
work order for the next scheduled modified perfo
rmance test and verifying battery 2C will remain operable until the next test scheduled for September 2013.  CENG also initiated
CR-2013-005074 to replace the two newly installed jars.
 
Analysis.  The inspectors determined that the failure to assure that the replacement of cells in battery 2C was prescribed and performed by appropriate procedures was a performance deficiency that was reasonably within CENG's ability to foresee and correct and should have been prevented.  This finding was more than minor because it was
associated with the equipment performance attribute of the Mitigating Systems  
cornerstone and affected the cornerstone objective of ensuring the availability, reliability,
and capability of systems that respond to initiating events to prevent undesirable consequences. 
In accordance with IMC 0609.04, "Initial Characterization of Findings," and Exhibit 2 of
IMC 0609, Appendix A, "The Significance Determination Process for Findings At-Power,"
issued June 19, 2012, the inspectors determined this finding to be of very low safety
significance (Green) because the performance deficiency was not a design or qualification deficiency, did not involve an actual loss of safety function, did not represent actual loss of a safety function of a single train for greater than its TS allowed outage
time, and did not screen as potentially risk significant due to a seismic, flooding, or
severe weather-initiating event.
 
This finding has a cross-cutting aspect in the area of Human Performance, Decision-
Making Component, because CENG did not use
conservative assumptions in decision making.  Specifically, CENG did not monitor the cells in storage, question the adequacy
of the discharged cells, charge the cells prior to installation, or fully evaluate the
implications of the test and recharge results [H.1(b)].
 
Enforcement.  10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," requires, in part, that activi
ties affecting quality shall be prescribed by documented instructions, procedures, or drawings of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, 
41  Enclosure procedures, or drawings.  Contrary to the above, CENG did not assure that the November 2012 replacement of cells in battery 2C was prescribed and performed by
appropriate procedures which resulted in degraded accuracy of test results and potential degradation to safety-related battery cells.  Because this violation was of very low safety significance (Green) and has been entered into CENG's CAP (CR-2013-005235), this
violation is being treated as an NCV, consistent with Section 2.3.2 of the NRC
 
Enforcement Policy.
  (NCV 05000410/2013003-02, Inadequate Procedural Implementation for Battery Cell Replacement)
    b.2 Inadequate Design Control for Battery 2C
  Introduction.  The inspectors identified a Green NCV of 10 CFR Part 50, Appendix B, Criterion III, "Design Control," because CENG did not verify the adequacy of the design
with respect to battery 2C.  Specifically, by failing to size the battery to the most limiting time period, the sizing calculation significantly overstated the available design margin.
Description.  The Division III emergency battery bank, battery 2C, uses jars that contain three cells each to provide reliable DC power for essential DC loads required during
normal and abnormal conditions at Unit 2.  The inspectors reviewed EC-145, "Verification of Adequacy of Division III Battery 2BYS*BAT2C," Revision 2, to determine if the calculation appropriately verified the adequacy of the size of the installed battery
2C.  The inspectors noted that the calculation evaluated the battery based on two time
periods, a 1-minute period and a 119-minute period.  In accordance with Institute of
Electrical and Electronics Engineers (IEEE) Standard 485-1997, "IEEE Recommended
Practice for Sizing Lead-Acid Batteries for Stationary Applications," and EC-145, the battery should be sized based upon the most demanding time period.  The inspectors determined that the sizing was incorrect.  Specifically, although EC-145 determined that
the first time period (1 minute) was the most demanding, the battery sizing was based
 
upon the less demanding second time period (119 minutes).
 
In response to this issue, CENG agreed that the calculation was incorrect, entered this issue into their CAP (CR-2013-005117), and evaluated the condition for operability. 
CENG performed the battery sizing calculation based upon the correct time period and
determined that the battery capacity margin reduced from 26 percent to negative
11 percent  (i.e., the battery was undersized by 11 percent).  CENG reduced the battery
design and aging margins from the calculation and were able to increase the capacity margin to positive 10 percent which demonstrated a reasonable expectation of operability.  The significance of reducing the design margin was that the original
calculation would have permitted modifications to the Division III DC system that could
have actually overloaded the battery.  The significance of reducing the aging margin is
that the battery would not have been able to perform its design function as the battery
aged.   
The inspectors independently performed battery sizing calculations and agreed with
CENG's results.
 
Analysis.  The inspectors determined that the failure to verify the adequacy of the design with respect to battery 2C was a performance deficiency that was reasonably within CENG's ability to foresee and correct and should have been prevented.  This finding was
more than minor because it was associated with the design control attribute of the 
42  Enclosure Mitigating Systems cornerstone and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to  
prevent undesirable consequences.  
In accordance with IMC 0609.04, "Initial Characterization of Findings," and Exhibit 2 of  
IMC 0609, Appendix A, "The Significance Determination Process for Findings At-Power,"
issued June 19, 2012, the inspectors determined this finding is of very low safety  
significance (Green) because the performance deficiency was not a design or qualification deficiency, did not involve an actual loss of safety function, did not represent actual loss of a safety function of a single train for greater than its TS allowed outage  
time, and did not screen as potentially risk-significant due to a seismic, flooding, or  
severe weather-initiating event.  
 
This finding did not have a cross-cutting aspect because it was not indicative of current performance. Specifically, EC-145 was last revised in 2008.  
 
Enforcement. 10 CFR 50, Appendix B, Criterion III, "Design Control," states, in part, that design control measures shall provide for verifying or checking the adequacy of design.
Contrary to the above, from July 17, 2008, to June 12, 2013, CENG's design control measures had not appropriately verified the adequacy of the design regarding battery 2C. Specifically, by failing to size the battery to the most limiting time period, the sizing calculation significantly overstated the available design margin. Because this violation  
was of very low safety significance (Green) and has been entered into CENG's CAP  
(CR-2013-005117), this violation is being treated as an NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy. (NCV 05000410/2013003-03, Inadequate Design Control for Battery Sizing Calculation)
4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153 - 6 samples)  
.1 Plant Events
 
   a. Inspection Scope
   a. Inspection Scope
 
    For the plant events listed below, the inspectors reviewed and/or observed plant
For the plant events listed below, the inspectors reviewed and/or observed plant  
    parameters, reviewed personnel performance, and evaluated performance of mitigating
parameters, reviewed personnel performance, and evaluated performance of mitigating systems. The inspectors communicated the plant events to appropriate regional personnel, and compared the event details with criteria contained in IMC 0309,  
    systems. The inspectors communicated the plant events to appropriate regional
"Reactive Inspection Decision Basis for Reactors," for consideration of potential reactive  
    personnel, and compared the event details with criteria contained in IMC 0309,
inspection activities. As applicable, the inspectors verified that CENG made appropriate  
    Reactive Inspection Decision Basis for Reactors, for consideration of potential reactive
emergency classification assessments and prop
    inspection activities. As applicable, the inspectors verified that CENG made appropriate
erly reported the event in accordance with 10 CFR Parts 50.72 and 50.73. The inspectors reviewed CENG's follow-up actions related to the events to assure that CENG implemented appropriate corrective actions  
    emergency classification assessments and properly reported the event in accordance
commensurate with their safety significance.  
    with 10 CFR Parts 50.72 and 50.73. The inspectors reviewed CENGs follow-up actions
  Unit 1 loss of battery board 12 and SDC on April 16, 2013 Loss of all SDC pumps for 17 minutes on April 16, 2013  
    related to the events to assure that CENG implemented appropriate corrective actions
 
    commensurate with their safety significance.
   
        Unit 1 loss of battery board 12 and SDC on April 16, 2013
43  Enclosure   b. Findings
        Loss of all SDC pumps for 17 minutes on April 16, 2013
  Introduction.  The inspectors documented an apparent violation of Unit 1 TS 6.4.1, "Procedures," because CENG failed to properly restore from a loss of a vital DC bus in accordance with station off-normal procedures resulting in an unplanned loss of all SDC
                                                                                          Enclosure
when time to boil was less than 2 hours.  Specifically, operators failed to recognize a
potential for loss of SDC during battery bus 12 restoration in accordance with N1-SOP-
47A.1, "Loss of DC," Revision 00101, and N1-OP-47A, "VDC Power System," Revision
 
02500.  Description.  Unit 1 shut down for a refueling outage on April 15, 2013.  On April 16, Unit 1 was in cold shutdown at 118 degrees Fahrenheit with a temperature band of 110
to 120 degrees Fahrenheit.  The reactor vessel head was installed, and the head bolts
were in the process of being detensioned in preparation for reactor cavity flood up and reactor vessel head removal.  Primary containment was open for planned maintenance.  Decay heat removal was via the SDC pump 12.  SDC pumps 11 and 13 were secured
with their breakers racked out to the test position for planned loss of offsite power/loss of
coolant accident testing (LOOP/LOCA).
 
During LOOP/LOCA testing, the SDC pumps and ECCS pumps in train associated with the bus are racked to their test position.  Operators are stationed in the field to restore
these pumps to normal so the pumps are still considered to be available.  This is


permitted by NMPNS TS's; however, automatic functions of the pumps are not available (such as auto start on a low-low reactor vessel level signal).  
                                            43
b. Findings
  Introduction. The inspectors documented an apparent violation of Unit 1 TS 6.4.1,
  Procedures, because CENG failed to properly restore from a loss of a vital DC bus in
  accordance with station off-normal procedures resulting in an unplanned loss of all SDC
  when time to boil was less than 2 hours. Specifically, operators failed to recognize a
  potential for loss of SDC during battery bus 12 restoration in accordance with N1-SOP-
  47A.1, Loss of DC, Revision 00101, and N1-OP-47A, VDC Power System, Revision
  02500.
  Description. Unit 1 shut down for a refueling outage on April 15, 2013. On April 16,
  Unit 1 was in cold shutdown at 118 degrees Fahrenheit with a temperature band of 110
  to 120 degrees Fahrenheit. The reactor vessel head was installed, and the head bolts
  were in the process of being detensioned in preparation for reactor cavity flood up and
  reactor vessel head removal. Primary containment was open for planned maintenance.
  Decay heat removal was via the SDC pump 12. SDC pumps 11 and 13 were secured
  with their breakers racked out to the test position for planned loss of offsite power/loss of
  coolant accident testing (LOOP/LOCA).
  During LOOP/LOCA testing, the SDC pumps and ECCS pumps in train associated with
  the bus are racked to their test position. Operators are stationed in the field to restore
  these pumps to normal so the pumps are still considered to be available. This is
  permitted by NMPNS TSs; however, automatic functions of the pumps are not available
  (such as auto start on a low-low reactor vessel level signal).
  At 2:45 p.m. on April 16, a contractor walking down a tagout associated with an ERV
  modification made an error and opened the breaker cabinet door for the vital DC bus 12.
  The vital DC bus 12 cabinet door contains a mechanical interlock which opens battery
  breaker 12 and the static battery charger DC output breaker, de-energizing the DC
  switchgear when the door is open. Upon opening the breaker cabinet door and hearing
  the breakers trip, the contractor realized he was in the incorrect cabinet and immediately
  contacted the control room and notified them of the event. The vital bus was considered
  protective equipment and a sign on the cabinet door cautioned that the door interlock
  would trip the breakers in that cabinet. The loss of the vital DC bus 12 resulted in a
  partial loss of indication in the main control room, loss of DC control power for the
  associated bus, and a high-temperature trip signal for the SDC 12 being generated.
  However, since DC power to the trip solenoid was also lost, the SDC pump 12 continued
  to run. The ECCS pumps associated with the #12 bus were inoperable due to loss of
  control power.
  In response to the event, operators entered procedure N1-SOP-47A, Loss of DC,
  Revision 00101. The flowchart in SOP-47A.1 directs the operator to transfer selected
  loads normally powered from battery bus 12 to their alternate power supplies and then
  directs restoration of the bus. However, a decision was made to not take actions
  specified in N1-SOP-47A.1 and pursue restoring the vital DC bus 12 using system
  operating procedure N1-OP-47A, 125 VDC Power System, Revision 02500. The
  inspectors noted that N1-SOP-47A.1 Section 5.1 contains two caution statements stating
  that pump trip signals may have been generated while the bus was de-energized and
  those signals must be cleared prior to restoration or a pump trip may occur when the bus
  is restored and power is supplied to the DC trip coils. However, neither N1-SOP-47A.1
  nor N1-OP-47A contained a list of tripping circuits and tripping actions which are
                                                                                      Enclosure


At 2:45 p.m. on April 16, a contractor walking down a tagout associated with an ERV modification made an error and opened the breaker cabinet door for the vital DC bus 12. 
                                          44
The vital DC bus 12 cabinet door contains a mechanical interlock which opens battery
associated with the vital DC bus 12. Operators failed to recognize the bus 12
breaker 12 and the static battery charger DC output breaker, de-energizing the DC
high-temperature trip signal present on the alarm log and the plant process computer
switchgear when the door is open.  Upon opening the breaker cabinet door and hearing the breakers trip, the contractor realized he was in the incorrect cabinet and immediately contacted the control room and notified them of the event.  The vital bus was considered
displays prior to attempting to restore bus 12. The presence of the trip signal was also
protective equipment and a sign on the cabinet door cautioned that the door interlock
indicated by a control room annunciator which was locked-in since the loss of battery
would trip the breakers in that cabinet.  The loss of the vital DC bus 12 resulted in a
bus 12 at 2:45 p.m.
partial loss of indication in the main control room, loss of DC control power for the
At 3:45 p.m., field operators attempted to close static battery charger 171A DC output
associated bus, and a high-temperature trip signal for the SDC 12 being generated.  However, since DC power to the trip solenoid was also lost, the SDC pump 12 continued to run.  The ECCS pumps associated with the #12 bus were inoperable due to loss of
breaker to restore the battery bus from its alternate power supply. Due to the high-
control power.
temperature trip signal already being present on the SDC pump 12, when operators
 
attempted to close the static battery charger 171A output breaker, the DC trip coil
received enough power to energize the relay and trip the SDC pump 12 just before the
In response to the event, operators entered procedure N1-SOP-47A, "Loss of DC," Revision 00101.  The flowchart in SOP-47A.1 directs the operator to transfer selected loads normally powered from battery bus 12 to their alternate power supplies and then
static battery charger 171A output breaker tripped due to the mechanical interlock.
directs restoration of the bus.  However, a decision was made to not take actions
Operators did not immediately recognize that they had lost SDC pump 12 via their
specified in N1-SOP-47A.1 and pursue restoring the vital DC bus 12 using system
indications at the control panel (i.e.; annunciator, pump current, pump flow). Upon
operating procedure N1-OP-47A, 125 "VDC Power System," Revision 02500.  The
recognizing the loss of SDC at approximately 3:50 p.m., operators entered N1-SOP-6.1
inspectors noted that N1-SOP-47A.1 Section 5.1 contains two caution statements stating that pump trip signals may have been generated while the bus was de-energized and those signals must be cleared prior to restoration or a pump trip may occur when the bus
Loss of SFP/RX Cavity Level/Decay Heat Removal, Revision 00501.
is restored and power is supplied to the DC trip coils.  However, neither N1-SOP-47A.1
At 3:50 p.m., the control room directed the breakers for SDC pumps 11 and 13 to be
nor N1-OP-47A contained a list of tripping circuits and tripping actions which are 
racked to their normal positions and that SDC be restored using the 11 and 13 SDC
44  Enclosure associated with the vital DC bus 12.  Operators failed to recognize the bus 12 high-temperature trip signal present on the alarm log and the plant process computer  
pumps. The 11 SDC pump breaker was restored at 4:03 pm and SDC flow was restored
displays prior to attempting to restore bus 12. The presence of the trip signal was also indicated by a control room annunciator which was locked-in since the loss of battery bus 12 at 2:45 p.m.  
at 4:17 pm when the SDC 11 temperature control valve was opened, restoring cooling
 
flow to the reactor. Reactor vessel temperature rose from 118 to 145 degrees
Fahrenheit as a result of the loss of SDC. At 5:11 p.m., the normal DC power
At 3:45 p.m., field operators attempted to close static battery charger 171A DC output  
distribution lineup was restored.
breaker to restore the battery bus from its alternate power supply. Due to the high-  
CENG immediately conducted prompt investigations of both the loss of battery bus 12
temperature trip signal already being present on the SDC pump 12, when operators attempted to close the static battery charger 171A output breaker, the DC trip coil received enough power to energize the relay and trip the SDC pump 12 just before the  
and loss of SDC events, entered both events into their CAP as CR-2013-002926 and
static battery charger 171A output breaker tripped due to the mechanical interlock.
CR-2013-002916, and conducted a root cause analysis. CENG determined the root
Operators did not immediately recognize that they had lost SDC pump 12 via their  
cause for the loss of SDC was inadequate procedural guidance for restoring the DC
indications at the control panel (i.e.; annunciator, pump current, pump flow). Upon recognizing the loss of SDC at approximately 3:50 p.m., operators entered N1-SOP-6.1 "Loss of SFP/RX Cavity Level/Decay Heat Removal," Revision 00501.  
power. Contributing causes included operators proceeding in the face of uncertainty,
 
management oversight of operations, and inadequate use of operational experience
which could have precluded this event. Corrective actions to prevent recurrence
At 3:50 p.m., the control room directed the breakers for SDC pumps 11 and 13 to be  
included a review of operations procedures to ensure those procedures contain
racked to their normal positions and that SDC be restored using the 11 and 13 SDC pumps. The 11 SDC pump breaker was restored at 4:03 pm and SDC flow was restored at 4:17 pm when the SDC 11 temperature control valve was opened, restoring cooling  
adequate levels of detail to safely recover from the event and restore the system to
flow to the reactor. Reactor vessel temperature rose from 118 to 145 degrees  
normal operation.
Fahrenheit as a result of the loss of SDC. At 5:11 p.m., the normal DC power  
Analysis. The inspectors determined that CENGs failure to properly restore the battery
distribution lineup was restored.  
bus 12 in accordance with plant procedures was a performance deficiency that was
 
reasonably within CENGs ability to foresee and correct and should have been
CENG immediately conducted prompt investigations of both the loss of battery bus 12 and loss of SDC events, entered both events into their CAP as CR-2013-002926 and  
prevented. The performance deficiency was determined to be more than minor because
CR-2013-002916, and conducted a root cause analysis. CENG determined the root  
the inspectors determined it affected the configuration control aspect of the Initiating
cause for the loss of SDC was inadequate procedural guidance for restoring the DC  
Events cornerstone and adversely affected the associated cornerstone objective to limit
power. Contributing causes included operators proceeding in the face of uncertainty, management oversight of operations, and inadequate use of operational experience which could have precluded this event. Corrective actions to prevent recurrence  
the likelihood of events that upset plant stability and challenge critical safety functions
included a review of operations procedures to ensure those procedures contain  
during shutdown as well as power operations. Specifically, operators failed to recognize
adequate levels of detail to safely recover from the event and restore the system to  
normal operation.  
 
Analysis. The inspectors determined that CENG's failure to properly restore the battery  
bus 12 in accordance with plant procedures was a performance deficiency that was reasonably within CENG's ability to foresee and correct and should have been  
prevented. The performance deficiency was determined to be more than minor because  
the inspectors determined it affected the configuration control aspect of the Initiating Events cornerstone and adversely affected the associated cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, operators failed to recognize  
a potential for loss of SDC during battery bus 12 restoration in accordance with N1-SOP-
a potential for loss of SDC during battery bus 12 restoration in accordance with N1-SOP-
47A.1, "Loss of DC," Revision 00101, and N1-OP-47A, "VDC Power System," Revision  
47A.1, Loss of DC, Revision 00101, and N1-OP-47A, VDC Power System, Revision
02500. This performance deficiency initiated a plant transient, loss of shutdown cooling.  
02500. This performance deficiency initiated a plant transient, loss of shutdown cooling.
The inspectors evaluated the finding using IMC 0609 Attachment 0609.04, "Initial  
The inspectors evaluated the finding using IMC 0609 Attachment 0609.04, Initial
Characterization of Findings," issued June 19, 2012, and IMC 0609 Appendix G,  
Characterization of Findings, issued June 19, 2012, and IMC 0609 Appendix G,
"Shutdown Operations Significance Determination Process," issued February 28, 2005.
Shutdown Operations Significance Determination Process, issued February 28, 2005.
45  Enclosure IMC 0609 Appendix G Table 1, "Losses of Control," states a quantitative analysis is required for:
                                                                                    Enclosure
 
  Loss of Thermal Margin (PWRs and BWRs)
  (Inadvertent change in RCS temperature due to loss of RHR)/(change in temperature that would cause boiling) > 0.2 (temperature margin to boil)
In this case, RCS temperature changed 27 degrees (145 to 118 degrees Fahrenheit)
and the change in temperature to boiling was 94 degrees (212 to 118 degrees
Fahrenheit).  Temperature margin to boil was greater than 0.2 (0.2872); thus, a quantitative analysis was required.  The significance of the finding is designated as To Be Determined (TBD) until a Phase 3 analysis can be completed by Regional and
 
Headquarters Senior Reactor Analysts.


                                              45
The inspectors determined this finding had a cross-cutting aspect in the area of Human Performance, Resources, because CENG did not ensure that personnel, equipment, procedures, and other resources were available and adequate to assure nuclear safety -  
    IMC 0609 Appendix G Table 1, Losses of Control, states a quantitative analysis is
complete, accurate and up-to-date design documentation, procedures, and work  
    required for:
packages, and correct labeling of components. Specifically, CENG procedures N1-SOP-47A.1 and N1-OP-47A did not contain adequate guidance to ensure recovery from a loss of a DC bus would not result in an unexpected plant transient [H.2(c)].
        Loss of Thermal Margin (PWRs and BWRs)
Enforcement. Unit 1 TS 6.4.1, "Procedures," requires, in part, that written procedures and administrative policies shall be established, implemented, and maintained that meet  
          (Inadvertent change in RCS temperature due to loss of RHR)/(change in temperature
or exceed the requirements and recommendations of Sections 5.1 and 5.3 of American  
          that would cause boiling) > 0.2 (temperature margin to boil)
National Standards Institute N18.7-1972
    In this case, RCS temperature changed 27 degrees (145 to 118 degrees Fahrenheit)
"Administrative Controls and Quality Assurance for the Operational Phase of Nuclear Power Plants," and cover the following activities: the applicable procedures recommended in RG 1.33, "Quality Assurance Program  
    and the change in temperature to boiling was 94 degrees (212 to 118 degrees
Requirements (Operation)," Appendix A, "Typical Procedures for Pressurized-Water  
    Fahrenheit). Temperature margin to boil was greater than 0.2 (0.2872); thus, a
Reactors and Boiling-Water Reactors," dated November 3, 1972. RG 1.33, Appendix A,  
    quantitative analysis was required. The significance of the finding is designated as To
Section 4, "Procedure for Startup, Operation, and Shutdown of Safety-Related BWR Systems," requires procedures for onsite DC system, and Section 6, "Procedures for Combating Emergencies and Other Significant Events," requires, in part, procedures for  
    Be Determined (TBD) until a Phase 3 analysis can be completed by Regional and
including loss of electrical power (and/or degraded power sources). CENG procedures  
    Headquarters Senior Reactor Analysts.
N1-OP-47A, "125 VDC Power System," Revision 02500, and N1-SOP-47A.1, "Loss of  
    The inspectors determined this finding had a cross-cutting aspect in the area of Human
DC," Revision 00101, implement this requirement. Contrary to the above, on April 16,  
    Performance, Resources, because CENG did not ensure that personnel, equipment,
2013, operators were unable to properly implement N1-OP-47 and N1-SOP-47A.1 following a loss of the battery bus 12 resulting in a temporary loss of all decay heat removal. This issue is being characterized as an apparent violation in accordance with  
    procedures, and other resources were available and adequate to assure nuclear safety -
the NRC's Enforcement Policy, and its final si
    complete, accurate and up-to-date design documentation, procedures, and work
gnificance will be dispositioned in a separate future correspondence. (Apparent Violation 05000220/2013003-04, Improper Bus Restoration Results in a Loss of Shutdown Cooling)
    packages, and correct labeling of components. Specifically, CENG procedures
  .2 (Closed) LER 05000220/2012-006-00: Technical Specification Required Shutdown Due to Containment Leakage  
    N1-SOP-47A.1 and N1-OP-47A did not contain adequate guidance to ensure recovery
    from a loss of a DC bus would not result in an unexpected plant transient [H.2(c)].
    Enforcement. Unit 1 TS 6.4.1, Procedures, requires, in part, that written procedures
    and administrative policies shall be established, implemented, and maintained that meet
    or exceed the requirements and recommendations of Sections 5.1 and 5.3 of American
    National Standards Institute N18.7-1972 Administrative Controls and Quality Assurance
    for the Operational Phase of Nuclear Power Plants, and cover the following activities:
    the applicable procedures recommended in RG 1.33, Quality Assurance Program
    Requirements (Operation), Appendix A, Typical Procedures for Pressurized-Water
    Reactors and Boiling-Water Reactors, dated November 3, 1972. RG 1.33, Appendix A,
    Section 4, Procedure for Startup, Operation, and Shutdown of Safety-Related BWR
    Systems, requires procedures for onsite DC system, and Section 6, Procedures for
    Combating Emergencies and Other Significant Events, requires, in part, procedures for
    including loss of electrical power (and/or degraded power sources). CENG procedures
    N1-OP-47A, 125 VDC Power System, Revision 02500, and N1-SOP-47A.1, Loss of
    DC, Revision 00101, implement this requirement. Contrary to the above, on April 16,
    2013, operators were unable to properly implement N1-OP-47 and N1-SOP-47A.1
    following a loss of the battery bus 12 resulting in a temporary loss of all decay heat
    removal. This issue is being characterized as an apparent violation in accordance with
    the NRC's Enforcement Policy, and its final significance will be dispositioned in a
    separate future correspondence. (Apparent Violation 05000220/2013003-04,
    Improper Bus Restoration Results in a Loss of Shutdown Cooling)
.2   (Closed) LER 05000220/2012-006-00: Technical Specification Required Shutdown Due
    to Containment Leakage
   a. Inspection Scope
   a. Inspection Scope
  On December 13, 2012, Unit 1 commenced a shutdown after observing nitrogen leakage  
    On December 13, 2012, Unit 1 commenced a shutdown after observing nitrogen leakage
from primary containment over a period of 10 days. NRC Inspection Report
    from primary containment over a period of 10 days. NRC Inspection Report
46  Enclosure 05000220/2012005 documented CENG's immediate response and the NRC's initial review of the event.  As of the end of the inspection documented in that report, CENG's
                                                                                      Enclosure
evaluation of the causes for the leakage was still ongoing.  The inspectors had identified an issue of concern regarding the total amount of leakage from primary containment vent and purge valves and its relation to exceeding the required value in TS 3.3.3.  The
NRC opened URI 05000220/2012005-03 to track CENG's completion of the root cause
evaluation, the quantification of the amount of leakage from primary containment for the event, and the NRC's subsequent review of CENG's completed evaluation.
To close URI 05000220/2012005-03 the inspectors reviewed and independently verified CENG's calculation regarding the quantity of leakage from primary containment from
December 3 - December 13.  The inspectors also reviewed Appendix J Type B and C
testing of the primary containment vent and purge valves to determine leakage
quantities and how they impacted overall primary containment leakage.  The inspectors also reviewed the cause of the leakage and CENG's actions to address the cause which was included in CR-2012-011157.  URI 05000220/2012005-03 is closed to the violation
discussed below.  The enforcement actions associated with this LER are discussed


below. This LER is closed.  
                                            46
  05000220/2012005 documented CENGs immediate response and the NRCs initial
  review of the event. As of the end of the inspection documented in that report, CENGs
  evaluation of the causes for the leakage was still ongoing. The inspectors had identified
  an issue of concern regarding the total amount of leakage from primary containment
  vent and purge valves and its relation to exceeding the required value in TS 3.3.3. The
  NRC opened URI 05000220/2012005-03 to track CENGs completion of the root cause
  evaluation, the quantification of the amount of leakage from primary containment for the
  event, and the NRCs subsequent review of CENGs completed evaluation.
  To close URI 05000220/2012005-03 the inspectors reviewed and independently verified
  CENGs calculation regarding the quantity of leakage from primary containment from
  December 3 - December 13. The inspectors also reviewed Appendix J Type B and C
  testing of the primary containment vent and purge valves to determine leakage
  quantities and how they impacted overall primary containment leakage. The inspectors
  also reviewed the cause of the leakage and CENGs actions to address the cause which
  was included in CR-2012-011157. URI 05000220/2012005-03 is closed to the violation
  discussed below. The enforcement actions associated with this LER are discussed
  below. This LER is closed.
b. Findings
  Introduction. A self-revealing Green NCV of TS 3.3.3, Leakage Rate, was identified for
  CENGs failure from December 3 to December 13, 2012, to maintain containment
  leakage less than 1.5 percent by weight of the containment air per day and less than 0.6
  percent by weight of the containment air per day for all penetrations and all primary
  containment isolation valves subject to 10 CFR Part 50, Appendix J, Types B and C
  tests, when pressurized to 35 pounds per square inch gauge (psig) when RCS
  temperature is above 215 degrees Fahrenheit and primary containment integrity is
  required.
  Description. On December 3, 2012, at 11:31 a.m., Unit 1 established primary
  containment integrity and commenced a reactor startup from an unplanned outage. The
  following day at 2:40 a.m., CENG operators commenced adding nitrogen gas into the
  primary containment as part of a planned activity to reduce primary containment oxygen
  concentration to less than 4 percent as required by TS 3.3.1, Oxygen Concentration.
  This activity was completed at 10:55 a.m. on December 4. Once an appropriate nitrogen
  concentration has been achieved in the containment, additional makeup is generally not
  required. However, from December 6 through December 8, on three occasions,
  operators added additional nitrogen to the containment to maintain pressure within
  procedural limits. This issue was documented in CR-2012-011157, Adverse Trend in
  Unit 1 Nitrogen Usage. CENG commenced initial troubleshooting activities which
  included examining systems and components that were possible sources of nitrogen
  leakage; however, a definitive source for the leakage was not identified. On
  December 12, following a fourth addition of nitrogen, CENG increased the importance of
  the issue, formed an issue response team, and staffed the outage control center. As
  part of the investigation process, operators cycled several containment isolation valves
  in the nitrogen purge and vent system and attempted to quantify the amount of seat
  leakage through the valves by opening test fittings located between isolation valves. In
  parallel with the troubleshooting efforts, CENG and vendor personnel began to develop
  analytical tools that could be used to quantify the amount of containment leakage.
                                                                                    Enclosure


  b. Findings
                                          47
  Introduction. A self-revealing Green NCV of TS 3.3.3, "Leakage Rate," was identified for CENG's failure from December 3 to December 13, 2012, to maintain containment leakage less than 1.5 percent by weight of the containment air per day and less than 0.6  
On December 13, at 6:47 p.m., after observing a decrease in containment pressure
percent by weight of the containment air per day for all penetrations and all primary containment isolation valves subject to 10 CFR Part 50, Appendix J, Types 'B' and 'C' tests, when pressurized to 35 pounds per square inch gauge (psig) when RCS  
following a fifth nitrogen addition and receiving preliminary data that a containment
temperature is above 215 degrees Fahrenheit  and primary containment integrity is  
isolation valve local leak-rate test between reactor containment inert gas purge and fill
required.  
drywell cooling system isolation valves IV-201-31 and IV-201-32 may fail, CENG
commenced a plant shutdown because primary containment integrity as required in TS
3.3.3 could not be assured. On December 13, at 11:33 p.m., the plant reached cold
shutdown and exited plant TS 3.3.3.
Subsequent testing of containment isolation valves revealed that three valves in the
reactor containment inert gas purge and fill drywell cooling system, valves IV-201-10,
IV-201-31, and IV-201-32 had unacceptable seat leak rates. These conditions were
documented in condition reports 2012-011210 and 2012-011288. When the valves were
disassembled and examined, CENG identified that iron oxide (i.e., rust) buildup on the
valve resilient seats had prevented the valves from closing tightly and adversely
impacted seat leakage performance. The reactor containment inert gas purge and fill
drywell cooling system is a carbon steel system and the internal piping surface adjacent
to the valves had visible signs of iron oxide degradation. CENG corrective actions
included removing the loose surface rust, installing new resilient seats on the valves,
and successfully performing as-left local leak-rate tests on the subject valves. Additional
corrective actions were outlined in CR-2012-011247.
CENG analysis determined that based upon the nitrogen supplied to the drywell,
containment leakage from December 3 through December 13, 2012, exceeded the limits
in TS 3.3.3 which requires containment leakage to be less than 1.5 percent by weight of
the containment air per day and less than 0.6 percent by weight of containment air per
day for all penetrations and all primary containment isolation valves subject to 10 CFR
Part 50, Appendix J, Types B and C tests, when pressurized to 35 psig when RCS
temperature is above 215°F and primary containment integrity is required. Specifically,
leakage was calculated to be between 1,421 and 2,023 standard cubic feet per hour
verses a calculated limit of 647 standard cubic feet per hour.
Analysis. The inspectors determined that CENGs failure to maintain containment
leakage from December 3 through December 13, 2012, within the limits required by TS
3.3.3 was a performance deficiency that was within CENGs ability to foresee and
correct and should have been prevented. This finding is more than minor because it is
associated with the SSC and barrier performance attribute of the Barrier Integrity
cornerstone and affected the cornerstone objective to provide reasonable assurance that
physical design barriers (fuel cladding, RCS, and containment) to protect the public from
radionuclide releases caused by accidents or events. Specifically, containment leakage
from December 3 through December 13 exceeded the leakage limits outlined in Unit 1
TS 3.3.3.
In accordance with IMC 0609.04, Initial Characterization of Findings, and Table 6.2,
Phase 2 Risk Significance-Type B Findings at Full Power, of IMC 0609, Appendix H,
Containment Integrity Significance Determination Process, issued May 6, 2004, the
inspectors determined this finding was of very low safety significance (Green) because
the leakage was less than 100 percent of containment volume per day for the duration of
the leak.
This finding has a cross-cutting aspect in the area of Problem Identification and
Resolution, CAP, because CENG failed to take appropriate corrective action to address
                                                                                  Enclosure


Description. On December 3, 2012, at 11:31 a.m., Unit 1 established primary containment integrity and commenced a reactor startup from an unplanned outage. The
                                              48
following day at 2:40 a.m., CENG operators commenced adding nitrogen gas into the  
  safety issues and adverse trends in a timely manner commensurate with their safety
primary containment as part of a planned activity to reduce primary containment oxygen
  significance. Specifically, following identification of the adverse trend regarding the
concentration to less than 4 percent as required by TS 3.3.1, "Oxygen Concentration.
  frequency of nitrogen addition to the drywell, CENG did not assess in a timely manner
This activity was completed at 10:55 a.m. on December 4. Once an appropriate nitrogen concentration has been achieved in the containment, additional makeup is generally not required. However, from December 6 through December 8, on three occasions,  
  the significance of the leakage and the impact on primary plant containment. As a
operators added additional nitrogen to the containment to maintain pressure within
  result, plant operation continued for several days with drywell leakage that exceeded the
  limits outlined in TS 3.3.3 [P.1(d)].
  Enforcement. TS 3.3.3, Leakage Rate, requires containment leakage to be less than
  1.5 percent by weight of the containment air per day and less than 0.6 percent by weight
  of the containment air per day for all penetrations and all primary containment isolation
  valves subject to 10 CFR Part 50, Appendix J, Types B and C tests, when pressurized
  to 35 psig when RCS temperature is above 215 degrees Fahrenheit and primary
  containment integrity is required. Contrary to the above, from December 3 through 13,
  2012, containment leakage exceeded 1.5 percent by weight. Specifically, following a
  December 13 plant shutdown, CENG determined containment leakage during this period
  to have been between 1,421 and 2,023 standard cubic feet per hour verses a calculated
  limit of 647. Because this violation is of very low safety significance (Green) and CENG
  entered this issue into their CAP as CR-2013-011247, this finding is being treated as an
  NCV consistent with consistent with Section 2.3.2 of the NRC Enforcement Policy.
  (NCV 05000220/2013003-05, Containment Leakage Exceeds Technical
  Specification 3.3.3 Limits)
.3 (Closed) LER 05000220/2012-006-01: Technical Specification Required Shutdown Due
  to Containment Leakage
  This LER was revised on June 14, 2013, to reflect changes in corrective actions that
  were outlined in the original LER submittal. In the original LER, CENG indicated that
  during the spring 2013 refueling outage, the internal surfaces of the horizontal drywell
  vent and purge piping that contained valves IV-201-09, IV-201-10, IV-201-31, and
  IV-201-32 would be coated with a material that would minimize the recurrence of rust
  buildup on the piping. Further, during the outage, the vertical piping that contained
  valves IV-201-07, IV-201-08, IV-201-16, and IV-201-17 would be inspected; and based
  on the inspection findings, a coating strategy (if required) would be developed for that
  piping. Subsequent to submittal of the original LER, CENG determined that based upon
  the difficultly associated with application of a suitable coating to the pipes and the
  potential of subsequent coating failure, a protective coating would not be installed.
  In lieu of the original corrective actions, CENG indicated that the horizontal section of
  pipe would be inspected each refueling outage. The vertical piping would not be
  inspected. These corrective actions were based, in part, on results from inspections
  conducted during the 2013 N1R22 that identified rust accumulation only on the
  horizontal sections of pipe. The enforcement aspects of this issue are discussed in
  section 4OA3.2 of this report. The inspectors did not identify any new issues during the
  review of this revised LER. This LER is closed.
.4 (Closed) LER 05000220/2012-007-00: High-Pressure Coolant Injection System Logic
  Actuation Following an Automatic Turbine Trip Signal due to High Reactor Water Level
  On November 6, 2012, while Unit 1 was in cold shutdown, an unexpected rise in reactor
  water level occurred causing an automatic turbine trip signal and actuation of the
  high-pressure coolant injection initiation logic. Operators immediately closed the 12
                                                                                      Enclosure


procedural limits. This issue was documented in CR-2012-011157, "Adverse Trend in Unit 1 Nitrogen Usage."  CENG commenced initial troubleshooting activities which included examining systems and components that were possible sources of nitrogen leakage; however, a definitive source for the leakage was not identified. On
                                              49
December 12, following a fourth addition of nitrogen, CENG increased the importance of  
  feedwater pump discharge blocking valve and stabilized reactor water level, stopping the
the issue, formed an issue response team, and staffed the outage control center. As
  transient. At Unit 1, high-pressure coolant injection is a mode of operation of the
part of the investigation process, operators
  condensate and feedwater system that utilizes the condensate storage tanks, main
cycled several containment isolation valves in the nitrogen purge and vent system and attempted to quantify the amount of seat leakage through the valves by opening test fittings located between isolation valves. In parallel with the troubleshooting efforts, CENG and vendor personnel began to develop
  condenser hotwell, two condensate pumps, two feedwater booster pumps, and two
analytical tools that could be used to quantify the amount of containment leakage.  
  motor-driven feedwater pumps. The rise in reactor water level resulted from the 12
  feedwater flow control valve (FCV) FCV-29-137 unexpectedly failing partially open when
  instrument air was removed from the valve during a tagout in preparation for
  maintenance on the valve. FCV-29-137 has a series of lockup valves that are designed
  to hold the FCV stem in position in the event instrument air is lost. CENG determined
  FCV-29-137 partially opened due to a degraded top cylinder lockup valve O-ring. The
  enforcement aspects of this issue are discussed in NRC Integrated Inspection Report
  05000220/2013002, Section 1R22. The inspectors did not identify any new issues
  during the review of the LER. This LER is closed.
.5 (Closed) LER 05000410/2013-001-00: Reactor Core Isolation Cooling System Isolation
  Due to a Temperature Switch Unit Failure
  On January 23, 2013, at 3:16 p.m., Unit 2 was operating at 100 percent power when an
  unexpected isolation signal for containment isolation valves in the RCIC and RHR
  system occurred due to a failure of a RB general area temperature switch
  (2RHS*TS85A). The isolation resulted in the RCIC system being unavailable for
  injection into the reactor vessel if called upon during an event. The affected RHR
  isolation valves were already in the closed position which is their normal position during
  power operation. The failure also occurred concurrently with the HPCS system being
  inoperable for planned surveillance testing. With both RCIC and HPCS inoperable,
  high-pressure coolant makeup capability was lost. At 3:50 p.m., HPCS was restored
  and declared operable. Temperature switch 2RHS*TS85A was replaced at 11:04 p.m.,
  and on January 24, at 1:17 a.m., RCIC was declared operable. The cause of the
  temperature switch failure was determined to be age-related capacitor degradation. The
  enforcement aspects of this issue are discussed in NRC Integrated Inspection Report
  05000410/2013002, Section 1R12. The inspectors did not identify any new issues
  during the review of the LER. This LER is closed.
.6 (Closed) LER 05000410/2013-002-00: Failure of High-Pressure Core Spray System
  Pressure Pump Due to Motor Winding Failure
  On February 28, 2013, Unit 2 was operating at 100 percent power when the HPCS
  system pressure pump failed. At the time of the failure, the HPCS system was
  inoperable for planned maintenance. The pump failure was due to turn-to-turn short in
  the motor winding. The HPCS system pressure pump is designed to maintain a positive
  pressure on the HPCS discharge header to prevent voids from forming. CENG replaced
  the HPCS pressure pump motor and returned the HPCS system to an operable status
  on March 6. The HPCS system discharge piping remained full during the period when
  the pressure pump was OOS. The inspectors reviewed the maintenance history of the
  HPCS pressure pump motor and determined that when the motor bearings were
  replaced in January 2011, the work order documented a satisfactory visual inspection
  and meggar testing of the motor windings. The inspectors reviewed the LER and
  determined that no findings or violations of NRC requirements were identified. This LER
  is closed.
                                                                                    Enclosure


 
                                              50
47  Enclosure On December 13, at 6:47 p.m., after observing a decrease in containment pressure following a fifth nitrogen addition and receiving preliminary data that a containment
4OA6 Meetings, Including Exit
isolation valve local leak-rate test betw
    Exit Meeting
een reactor containment inert gas purge and fill
    On July 25, 2013, the inspectors presented the inspection results to Mr. Christopher
drywell cooling system isolation valv
    Costanzo, Site Vice President, and other members of the NMPNS staff. The inspectors
es IV-201-31 and IV-201-32 may fail, CENG commenced a plant shutdown because primary containment integrity as required in TS
    verified that no propriety information was retained by the inspectors or documented in
3.3.3 could not be assured.  On December 13, at 11:33 p.m., the plant reached cold
    this report.
ATTACHMENT: SUPPLEMENTARY INFORMATION
                                                                                    Enclosure


shutdown and exited plant TS 3.3.3.  
                                              A-1
                              SUPPLEMENTARY INFORMATION
                                  KEY POINTS OF CONTACT
Licensee Personnel
C. Costanzo, Vice President
J. Stanley, Plant General Manager
P. Bartolini, Supervisor, Design Engineering
K. Clark, Director, Security
S. Dack, Seasonal Readiness Coordinator / Cycle Manager
J. Dean, Supervisor, Quality Assurance
S. Dhar, Design Engineering
J. Dosa, Director, Licensing
J. Gillard, Emergency Preparedness Analyst
J. Holton, Supervisor, Systems Engineering
G. Inch, Principle Engineer,
M. Kunzwiler, Security Supervisor
J. Leonard, Supervisor Design Engineering
C. McClay, Senior Engineer
F. Payne, Manager, Operations
P. Politzi, Work Week Manager
J. Reid, Design Engineer
B. Scaglione, System Engineer
J. Schulz, System Engineer
M. Shanbhag, Licensing Engineer
R. Staley, System Engineer
T. Syrell, Manager, Nuclear Safety and Security
J. Thompson, General Supervisor, Mechanical Maintenance
A. Verno, Director, Emergency Preparedness
                                                        Attachment


                                      A-2
Subsequent testing of containment isolation valves revealed that three valves in the reactor containment inert gas purge and fill drywell cooling system, valves IV-201-10, IV-201-31, and IV-201-32 had unacceptable seat leak rates.  These conditions were
            LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED
documented in condition reports 2012-011210 and 2012-011288.  When the valves were
Opened
disassembled and examined, CENG identified that iron oxide (i.e., rust) buildup on the
05000220/2013003-04      AV        Improper Bus Restoration Results in a Loss of
valve resilient seats had prevented the va
                                    Shutdown Cooling (Section 4OA3)
lves from closing
Opened/Closed
tightly and adversely impacted seat leakage performance.  The reactor containment inert gas purge and fill drywell cooling system is a carbon steel system and the internal piping surface adjacent to the valves had visible signs of iron oxide degradation.  CENG corrective actions
05000410/2013003-01      NCV        Failure to Follow Containment Isolation System
included removing the loose surface rust, installing new resilient seats on the valves,
                                    Surveillance Procedure Resulting in Isolation of the
and successfully performing as-left local leak-rate tests on the subject valves.  Additional corrective actions were outlined in CR-2012-011247.
                                    Reactor Coolant Isolation Cooling System
                                    (Section 1R22)
CENG analysis determined that based upon the nitrogen supplied to the drywell,
05000410/2013003-02      NCV        Inadequate Procedural Implementation for Battery
containment leakage from December 3 through December 13, 2012, exceeded the limits
                                    Cell Replacement (Section 4OA2)
in TS 3.3.3 which requires containment leakage to be less than 1.5 percent by weight of
05000410/2013003-03      NCV        Inadequate Design Control for Battery Sizing
the containment air per day and less than 0.6 percent by weight of containment air per day for all penetrations and all primary containment isolation valves subject to 10 CFR Part 50, Appendix J, Types 'B' and 'C' tests, when pressurized to 35 psig when RCS 
                                    Calculation (Section 4OA2)
temperature is above 215°F and primary containment integrity is required.  Specifically, leakage was calculated to be between 1,421 and 2,023 standard cubic feet per hour
05000220/2013003-05      NCV        Containment Leakage Exceeds Technical
verses a calculated limit of 647 standard cubic feet per hour. 
                                    Specification 3.3.3 Limits (Section 4OA3)
Analysis.  The inspectors determined that CENG's failure to maintain containment leakage from December 3 through December 13, 2012, within the limits required by TS
Closed
3.3.3 was a performance deficiency that was within CENG's ability to foresee and  
05000220/2012005-03      URI        Assessment of Containment Leakage Due to
correct and should have been prevented.  This finding is more than minor because it is
                                    Containment Isolation Valve Failure (4OA3)
associated with the SSC and barrier performance attribute of the Barrier Integrity cornerstone and affected the cornerstone objective to provide reasonable assurance that physical design barriers (fuel cladding, RCS, and containment) to protect the public from
05000220/2012-006-00 and LER        Technical Specification Required Shutdown Due
radionuclide releases caused by accidents or
05000220/2012-006-01                to Containment Leakage (Section 4OA3)
events.  Specifically, containment leakage
05000220/2012-007-00    LER        High-Pressure Coolant Injection System Logic
from December 3 through December 13 exceeded the leakage limits outlined in Unit 1
                                    Actuation Following an Automatic Turbine Trip
TS 3.3.3.
                                    Signal Due to High Reactor Water Level
In accordance with IMC 0609.04, "Initial Characterization of Findings," and Table 6.2,
                                    (Section 4OA3)
"Phase 2 Risk Significance-Type B Findings at Full Power," of IMC 0609, Appendix H,
05000410/2013-001-00    LER        Reactor Core Isolation Cooling System Isolation
"Containment Integrity Significance Determination Process," issued May 6, 2004, the
                                    Due to a Temperature Switch Unit Failure
inspectors determined this finding was of very low safety significance (Green) because
                                    (Section 4OA3)
the leakage was less than 100 percent of containment volume per day for the duration of the leak. 
05000410/2013-002-00    LER        Failure of High-Pressure Core Spray System
This finding has a cross-cutting aspect in the area of Problem Identification and
                                    Pressure Pump Due to Motor Winding Failure
Resolution, CAP, because CENG failed to take appropriate corrective action to address 
                                    (Section 4OA3)
48  Enclosure safety issues and adverse trends in a timely manner commensurate with their safety significance.  Specifically, following identification of the adverse trend regarding the frequency of nitrogen addition to the drywell, CENG did not assess in a timely manner the significance of the leakage and the impact on primary plant containment.  As a result, plant operation continued for several days with drywell leakage that exceeded the
                                                                              Attachment
limits outlined in TS 3.3.3 [P.1(d)]. 


                                            A-3
Enforcement.  TS 3.3.3, "Leakage Rate," requires containment leakage to be less than 1.5 percent by weight of the containment air per day and less than 0.6 percent by weight
                              LIST OF DOCUMENTS REVIEWED
of the containment air per day for all penetra
Section 1R01: Adverse Weather Protection
tions and all primary containment isolation valves subject to 10 CFR Part 50, Appendix J, Types 'B' and 'C' tests, when pressurized
Procedures
to 35 psig when RCS temperature is above 215 degrees Fahrenheit and primary
N1-OP-64, Meteorological Monitoring, Revision 00603
containment integrity is required.  Contrary to the above, from December 3 through 13,  
N2-OP-102, Meteorological Monitoring, Revision 01103
2012, containment leakage exceeded 1.5 percent
N2-OP-102, Attachment 3, Hot Weather Preparation Checklist, Revision 01102
by weight.  Specifically, following a December 13 plant shutdown, CENG determined containment leakage during this period to have been between 1,421 and 2,023 standard cubic feet per hour verses a calculated
NAI-PSH-11, Seasonal Readiness Program, Revision 00700
limit of 647.  Because this violation is of very low safety significance (Green) and CENG entered this issue into their CAP as CR-2013-011247, this finding is being treated as an
Condition Reports
NCV consistent with consistent with Sect
CR-2010-008430                    CR-2011-010519                  CR-2012-004448
ion 2.3.2 of the NRC Enforcement Policy.  (NCV 05000220/2013003-05, Containment Leakage Exceeds Technical
CR-2011-008564                    CR-2012-001034                  CR-2012-007341
Specification 3.3.3 Limits)
CR-2011-009058                    CR-2012-002008                  CR-2013-000154
  .3 (Closed) LER 05000220/2012-006-01:  Technical Specification Required Shutdown Due to Containment Leakage
CR-2011-009946                    CR-2012-004258
Work Orders
WO C90679919                      WO C91901545                    WO C92110489
WO C91178423                      WO C91919260                    WO C92116209
WO C91425002                      WO C91920244                    WO C92133487
WO C91570604                      WO C91966877                    WO C92135500
WO C91570606                      WO C92033133                    WO C92139868
WO C91711577                      WO C92008152                    WO C92154168
WO C91847825                      WO C92008169                    WO C92156668
WO C91860534                      WO C92015166                    WO C92156894
WO C91862547                      WO C92044771                    WO C92161257
WO C91862559                      WO C92067054                    WO C92221738
WO C91883258                      WO C92073630                    WO C92226912
WO C91883511                      WO C92073671                    WO C92285675
WO C91883613                      WO C92073704                    WO C92292596
WO C91897710                      WO C92107827
Miscellaneous
Diesel Trend Analysis
Summer Readiness Status, Attachment 1
System Seasonal Readiness Evaluations, Attachment 2
Unit 1 Scheduler Evaluation for Summer Readiness from June 15 to September 15
Unit 2 Scheduler Evaluation for Summer Readiness from June 15 to September 15
Section 1R04: Equipment Alignment
Procedures
N1-OP-13, Emergency Cooling System, Revision 03700
N1-OP-48, Control Room Ventilation System, Revision 02400
NIP-OUT-01, Shutdown Safety, Revision 03700
                                                                                Attachment


This LER was revised on June 14, 2013, to reflect changes in corrective actions that were outlined in the original LER submittal.  In the original LER, CENG indicated that
                                              A-4
during the spring 2013 refueling outage, the internal surfaces of the horizontal drywell
Condition Reports
vent and purge piping that contained valves IV-201-09, IV-201-10, IV-201-31, and
CR-2013-004333
IV-201-32 would be coated with a material that would minimize the recurrence of rust buildup on the piping.  Further, during the outage, the vertical piping that contained valves IV-201-07, IV-201-08, IV-201-16, and IV-201-17 would be inspected; and based
CR-2013-004347
on the inspection findings, a coating strategy (if required) would be developed for that
Drawings
piping.  Subsequent to submittal of the original LER, CENG determined that based upon
B-69017-C, Emergency Condenser Number 11 Steam Flow, Revision 1
the difficultly associated with application of a suitable coating to the pipes and the
C-180007-C, Reactor Core Spray Piping and Instrumentation Drawing (P&ID), Revision 58
potential of subsequent coating failure, a protective coating would not be installed. 
C-18008-C, Spent Fuel Storage Pool Filtering and Cooling System, Revision 38
In lieu of the original corrective actions, CENG indicated that the horizontal section of
C-18030-C, Fire Protection Water System, Revision 38
pipe would be inspected each refueling outage.  The vertical piping would not be
C-18047-C, Control Room Heating Ventilation and Air Conditioning System, Revision 48
inspected.  These corrective actions were based, in part, on results from inspections
C-181017-C, Emergency Cooling System, Revision, Revision 55
conducted during the 2013 N1R22 that identified rust accumulation only on the horizontal sections of pipe.  The enforcement aspects of this issue are discussed in section 4OA3.2 of this report.  The inspectors did not identify any new issues during the
Miscellaneous
review of this revised LER.  This LER is closed.
Plant Configuration Change 1M00888
Section 1R05: Fire Protection
.4 (Closed) LER 05000220/2012-007-00:  High-Pressure Coolant Injection System Logic  Actuation Following an Automatic Turbine Trip Signal due to High Reactor Water Level
Procedure
On November 6, 2012, while Unit 1 was in cold shutdown, an unexpected rise in reactor
N1-PFP-0101, Unit 1 Pre-Fire Plans, Revision 00200
water level occurred causing an automatic turbine trip signal and actuation of the
Condition Report
high-pressure coolant injection initiation logic.  Operators immediately closed the 12 
CR-2013-002902
49  Enclosure feedwater pump discharge blocking valve and stabilized reactor water level, stopping the transient.  At Unit 1, high-pressure coolant injection is a mode of operation of the
Miscellaneous
condensate and feedwater system that utilizes the condensate storage tanks, main condenser hotwell, two condensate pumps, two feedwater booster pumps, and two motor-driven feedwater pumps.  The rise in reactor water level resulted from the 12
USAR Section 10, Revision 16
feedwater flow control valve (FCV) FCV-29-137 unexpectedly failing partially open when
Section 1R07: Heat Sink Performance
instrument air was removed from the valve during a tagout in preparation for
Procedure
maintenance on the valve.  FCV-29-137 has a series of lockup valves that are designed
N1-ST-Q25, Emergency Diesel Generator Cooling Water Quarterly Test, Revision 02201
to hold the FCV stem in position in the event instrument air is lost.  CENG determined FCV-29-137 partially opened due to a degraded top cylinder lockup valve O-ring.  The enforcement aspects of this issue are discussed in NRC Integrated Inspection Report
Work Order
05000220/2013002, Section 1R22.  The inspectors did not identify any new issues
WO C91454468
during the review of the LER.  This LER is closed.
Section 1R08: In-Service Inspection
.5 (Closed) LER 05000410/2013-001-00:  Reactor Core Isolation Cooling System Isolation Due to a Temperature Switch Unit Failure
Procedures
NDEP-PT-3.00, Liquid Penetrant Examination, Revision 01900
On January 23, 2013, at 3:16 p.m., Unit 2 was operating at 100 percent power when an unexpected isolation signal for containment isolation valves in the RCIC and RHR system occurred due to a failure of a RB general area temperature switch (2RHS*TS85A).  The isolation resulted in the RCIC system being unavailable for
NDEP-UT-6.23, UT Examination of Ferritic Piping Welds, Revision 01100
injection into the reactor vessel if called upon during an event.  The affected RHR
NDEP-UT-6.24, UT Examination of Austenitic Piping Welds, Revision 01101
isolation valves were already in the closed position which is their normal position during
NDEP-VT-2.01, ASME Section XI Visual Examination, Revision 19
power operation.  The failure also occurred concurrently with the HPCS system being
NDEP-VT-2.07, In-Vessel Visual Examination, Revision 1300
inoperable for planned surveillance testing.  With both RCIC and HPCS inoperable, high-pressure coolant makeup capability was lost.  At 3:50 p.m., HPCS was restored and declared operable.  Temperature switch 2RHS*TS85A was replaced at 11:04 p.m.,
NIP-IIT-02, ASME Section XI Repair and Replacement Program, Revision 00701
and on January 24, at 1:17 a.m., RCIC was declared operable.  The cause of the
SI-UT-130, Phased Array Ultrasonic Examination of Dissimilar Metal Welds, Revision 0
temperature switch failure was determined to be age-related capacitor degradation. The
Condition Reports
enforcement aspects of this issue are discussed in NRC Integrated Inspection Report 05000410/2013002, Section 1R12.  The inspectors did not identify any new issues during the review of the LER.  This LER is closed.
CR-2012-000816
                                                                                    Attachment
.6 (Closed) LER 05000410/2013-002-00:  Failure of High-Pressure Core Spray System Pressure Pump Due to Motor Winding Failure
 
On February 28, 2013, Unit 2 was operating at 100 percent power when the HPCS system pressure pump failed. At the time of the failure, the HPCS system was
inoperable for planned maintenance.  The pump failure was due to turn-to-turn short in
the motor winding.  The HPCS system pressure pump is designed to maintain a positive
pressure on the HPCS discharge header to prevent voids from forming.  CENG replaced the HPCS pressure pump motor and returned the HPCS system to an operable status on March 6. The HPCS system discharge piping remained full during the period when
the pressure pump was OOS.  The inspectors reviewed the maintenance history of the
HPCS pressure pump motor and determined that when the motor bearings were
replaced in January 2011, the work order documented a satisfactory visual inspection
and meggar testing of the motor windings.  The inspectors reviewed the LER and
determined that no findings or violations of NRC requirements were identified.  This LER is closed. 
 
50  Enclosure 4OA6 Meetings, Including Exit
  Exit Meeting
  On July 25, 2013, the inspectors presented the inspection results to Mr. Christopher
Costanzo, Site Vice President, and other members of the NMPNS staff.  The inspectors
verified that no propriety information was retained by the inspectors or documented in
this report.  
  ATTACHMENT:  SUPPLEMENTARY INFORMATION
 
Attachment
A-1 SUPPLEMENTARY INFORMATION
  KEY POINTS OF CONTACT
Licensee Personnel
 
C. Costanzo, Vice President
J. Stanley, Plant General Manager P. Bartolini, Supervisor, Design Engineering
K. Clark, Director, Security 
S. Dack, Seasonal Readiness Coordinator / Cycle Manager 
 
J. Dean, Supervisor, Quality Assurance S. Dhar, Design Engineering J. Dosa, Director, Licensing
J. Gillard, Emergency Preparedness Analyst


J. Holton, Supervisor, Systems Engineering
                                              A-5
G. Inch, Principle Engineer, 
CR-2012-003805
M. Kunzwiler, Security Supervisor  J. Leonard, Supervisor Design Engineering
CR-2012-010291
C. McClay, Senior Engineer
CR-2013-000506
 
CR-2013-001573
F. Payne, Manager, Operations
P. Politzi, Work Week Manager
J. Reid, Design Engineer B. Scaglione, System Engineer J. Schulz, System Engineer
M. Shanbhag, Licensing Engineer
R. Staley, System Engineer
 
T. Syrell, Manager, Nuclear Safety and Security J. Thompson, General Supervisor, Mechanical Maintenance
A. Verno, Director, Emergency Preparedness
 
 
Attachment
A-2 LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED
Opened 
05000220/2013003-04
AV  Improper Bus Restoration Results in a Loss of      Shutdown Cooling (Section 4OA3)
Opened/Closed
 
05000410/2013003-01 NCV  Failure to Follow Containment Isolation System  Surveillance Procedure Resulting in Isolation of the
Reactor Coolant Isolation Cooling System (Section 1R22)
05000410/2013003-02 NCV  Inadequate Procedural Implementation for Battery
      Cell Replacement (Section 4OA2)
 
05000410/2013003-03 NCV  Inadequate Design Control for Battery Sizing      Calculation (Section 4OA2)
 
05000220/2013003-05 NCV  Containment Leakage Exceeds Technical  Specification 3.3.3 Limits (Section 4OA3)
Closed  05000220/2012005-03 URI  Assessment of Containment Leakage Due to  Containment Isolation Valve Failure (4OA3)
05000220/2012-006-00 and LER  Technical Specification Required Shutdown Due 05000220/2012-006-01  to Containment Leakage (Section 4OA3)
05000220/2012-007-00 LER  High-Pressure Coolant Injection System Logic
      Actuation Following an Automatic Turbine Trip
      Signal Due to High Reactor Water Level 
      (Section 4OA3)
05000410/2013-001-00 LER  Reactor Core Isolation Cooling System Isolation
      Due to a Temperature Switch Unit Failure 
      (Section 4OA3)
 
05000410/2013-002-00 LER  Failure of High-Pressure Core Spray System        Pressure Pump Due to Motor Winding Failure
      (Section 4OA3) 
 
 
 
Attachment
A-3 LIST OF DOCUMENTS REVIEWED
  Section 1R01:  Adverse Weather Protection
  Procedures
N1-OP-64, Meteorological Monitoring, Revision 00603 N2-OP-102, Meteorological Monitoring, Revision 01103 N2-OP-102, Attachment 3, Hot Weather Preparation Checklist, Revision 01102 NAI-PSH-11, Seasonal Readiness Program, Revision 00700
Condition Reports
CR-2010-008430 CR-2011-008564 CR-2011-009058
CR-2011-009946 CR-2011-010519 CR-2012-001034
CR-2012-002008
CR-2012-004258 CR-2012-004448 CR-2012-007341 CR-2013-000154
Work Orders
WO C90679919 WO C91178423 WO C91425002 WO C91570604
WO C91570606
WO C91711577
WO C91847825 WO C91860534 WO C91862547
WO C91862559
WO C91883258
WO C91883511
WO C91883613 WO C91897710 WO C91901545 WO C91919260 WO C91920244 WO C91966877
WO C92033133
WO C92008152
WO C92008169 WO C92015166 WO C92044771
WO C92067054
WO C92073630
WO C92073671
WO C92073704 WO C92107827 WO C92110489 WO C92116209 WO C92133487 WO C92135500
WO C92139868
WO C92154168
WO C92156668 WO C92156894 WO C92161257
WO C92221738
WO C92226912
WO C92285675
WO C92292596
Miscellaneous
Diesel Trend Analysis Summer Readiness Status, Attachment 1 System Seasonal Readiness Evaluations, Attachment 2  Unit 1 Scheduler Evaluation for Summer Readiness from June 15 to September 15 Unit 2 Scheduler Evaluation for Summer Readiness from June 15 to September 15
Section 1R04:  Equipment Alignment
  Procedures
N1-OP-13, Emergency Cooling System, Revision 03700  N1-OP-48, Control Room Ventilation System, Revision 02400 NIP-OUT-01, Shutdown Safety, Revision 03700
 
Attachment
A-4 Condition Reports
CR-2013-004333 CR-2013-004347
Drawings B-69017-C, Emergency Condenser Number 11 Steam Flow, Revision 1  C-180007-C, Reactor Core Spray Piping and Instrumentation Drawing (P&ID), Revision 58 C-18008-C, Spent Fuel Storage Pool Filtering and Cooling System, Revision 38  C-18030-C, Fire Protection Water System, Revision 38  C-18047-C, Control Room Heating Ventilation and Air Conditioning System, Revision 48 
C-181017-C, Emergency Cooling System, Revision, Revision 55
Miscellaneous
Plant Configuration Change 1M00888 
Section 1R05:  Fire Protection
  Procedure N1-PFP-0101, Unit 1 Pre-Fire Plans, Revision 00200
Condition Report
CR-2013-002902
Miscellaneous
USAR Section 10, Revision 16
Section 1R07:  Heat Sink Performance
  Procedure N1-ST-Q25, Emergency Diesel Generator Cooling Water Quarterly Test, Revision 02201
Work Order
WO C91454468
Section 1R08:  In-Service Inspection
  Procedures
NDEP-PT-3.00, Liquid Penetrant Examination, Revision 01900
NDEP-UT-6.23, UT Examination of Ferritic Piping Welds, Revision 01100
NDEP-UT-6.24, UT Examination of Austenitic Piping Welds, Revision 01101
NDEP-VT-2.01, ASME Section XI Visual Examination, Revision 19
NDEP-VT-2.07, In-Vessel Visual Examination, Revision 1300 NIP-IIT-02, ASME Section XI Repair and Replacement Program, Revision 00701 SI-UT-130, Phased Array Ultrasonic Examination of Dissimilar Metal Welds, Revision 0
 
Condition Reports
CR-2012-000816 
Attachment
A-5CR-2012-003805 CR-2012-010291  
CR-2013-000506  
CR-2013-001573  
CR-2013-002975
CR-2013-002975
CR-2013-002977
CR-2013-002977
CR-2013-002978  
CR-2013-002978
CR-2013-003442  
CR-2013-003442
 
Drawing
C-18009, Reactor Water Cleanup P&ID, Revision 60, Sheet 1
Drawing C-18009, Reactor Water Cleanup P&ID, Revision 60, Sheet 1  
Work Order
Work Order
WO C92260831  
WO C92260831
 
NDE Records
NDE Records
BOP-UT-13-014, UT Calibration/Thickness Examination Records of RBCLC System Piping to Recirculation Pump 11 Motor MOT-32-187, dated April 21, 2013  
BOP-UT-13-014, UT Calibration/Thickness Examination Records of RBCLC System Piping to
 
      Recirculation Pump 11 Motor MOT-32-187, dated April 21, 2013
BOP-UT-13-015, UT Calibration/Thickness Examination Records of RBCLC System Piping to Recirculation Pump 12 Motor MOT-32-188, dated April 21, 2013  
BOP-UT-13-015, UT Calibration/Thickness Examination Records of RBCLC System Piping to
      Recirculation Pump 12 Motor MOT-32-188, dated April 21, 2013
BOP-UT-13-016, UT Calibration/Thickness Examination Records of RBCLC System Piping to
      Recirculation Pump 13 Motor MOT-32-189, dated April 21, 2013
BOP-UT-13-017, UT Calibration/Thickness Examination Records of RBCLC System Piping to
      Recirculation Pump 14 Motor MOT-32-190, dated April 21, 2013
BOP-UT-13-018, UT Calibration/Thickness Examination Records of RBCLC System Piping to
      Recirculation Pump 15 Motor MOT-32-191, dated April 21, 2013
BOP-UT-13-021, UT Calibration/Thickness Examination Records of General Corrosion of
      RBCLC System Piping Inside U1 Drywell 225 Feet Elevation, dated April 24, 2013
ISI-PT-13-003, Liquid Penetrant Examination Record of Branch Connection - Decontamination
      Port Weld 32-WD-011 on Recirculation System Suction Piping, dated April 24, 2013
ISI-PT-13-004, Liquid Penetrant Examination Record of Branch Connection - Decontamination
      Port Weld 32-WD-091 on Recirculation System Suction Piping, dated April 24, 2013
ISI-UT-13-032, UT Calibration/Examination Records of Branch Connection - Decontamination
      Port Weld 32-WD-051 on Recirculation System Suction Piping, dated April 22, 2013
ISI-UT-13-033, UT Calibration/Examination Records of 12-Inch Diameter Emergency Condenser
      Supply Piping, Pipe-to-Pipe Weld 39-WD-108, dated April 24, 2013
ISI-UT-13-034, UT Calibration/Examination Records of 12-Inch Diameter Emergency Condenser
      Supply Piping, Pipe-to-Tee Weld 39-WD-109, dated April 24, 2013
ISI-UT-13-035, UT Calibration/Examination records of 12-Inch Diameter Emergency Condenser
      Supply Piping, Tee-to-Pipe Weld 39-WD-110, dated April 24, 2013
ISI-UT-13-036, UT Calibration/Examination Records of 12-Inch Diameter Emergency Condenser
      Supply Piping, Pipe-to-Elbow Weld 39-WD-112, dated April 20, 2013
NMP U1 33-WD-046, Phased Array UT Calibration/Examination Records of 6-Inch Diameter
      RBCLC Pipe-to-Pipe DM Weld, dated April 29, 2013
UT Calibration/Examination Records of Unit 1 32-WD-042, N2A Safe End-Nozzle DM Weld,
      Phased Array Ultrasonic Examination Record, dated April 30, 2013
UT Calibration/Examination Records of Unit 1 32-WD-042, N2A Safe End-to-Nozzle DM Weld
      on Recirc Discharge, Phased Array Ultrasonic Examination Record, dated April 30, 2013
UT Calibration/Examination Records of Unit 1 32-WD-082, N2B Safe End-to-Nozzle DM Weld
      on Recirc Discharge, Phased Array Ultrasonic Examination Record, dated April 30, 2013
                                                                                  Attachment


BOP-UT-13-016, UT Calibration/Thickness Examination Records of RBCLC System Piping to  Recirculation Pump 13 Motor MOT-32-189, dated April 21, 2013
                                              A-6
BOP-UT-13-017, UT Calibration/Thickness Examination Records of RBCLC System Piping to  Recirculation Pump 14 Motor MOT-32-190, dated April 21, 2013
UT Calibration/Examination Records of Uni5 1 32-WD-122, N2C Safe End-to-Nozzle DM Weld
 
      on Recirc Discharge, Phased Array Ultrasonic Examination Record, dated April 30, 2013
BOP-UT-13-018, UT Calibration/Thickness Examination Records of RBCLC System Piping to  Recirculation Pump 15 Motor MOT-32-191, dated April 21, 2013
UT Calibration/Examination Records of Unit 1 32-WD-164, N2D Safe End-to-Nozzle DM Weld
BOP-UT-13-021, UT Calibration/Thickness Examination Records of General Corrosion of  RBCLC System Piping Inside U1 Drywell 225 Feet Elevation, dated April 24, 2013 ISI-PT-13-003, Liquid Penetrant Examination Record of Branch Connection - Decontamination
      on Recirc Discharge, Phased Array Ultrasonic Examination Record, dated April 30, 2013
Port Weld 32-WD-011 on Recirculation System Suction Piping, dated April 24, 2013
UT Calibration/Examination Records of Unit 1 32-WD-208, N2E Safe End-to-Nozzle DM Weld
ISI-PT-13-004, Liquid Penetrant Examination Record of Branch Connection - Decontamination
      on Recirc Discharge, Phased Array Ultrasonic Examination Record, dated April 30, 2013
Port Weld 32-WD-091 on Recirculation System Suction Piping, dated April 24, 2013 ISI-UT-13-032, UT Calibration/Examination Records of Branch Connection - Decontamination  Port Weld 32-WD-051 on Recirculation System Suction Piping, dated April 22, 2013
ISI-UT-13-033, UT Calibration/Examination Records of 12-Inch Diameter Emergency Condenser
Supply Piping, Pipe-to-Pipe Weld 39-WD-108, dated April 24, 2013
ISI-UT-13-034, UT Calibration/Examination Records of 12-Inch Diameter Emergency Condenser
Supply Piping, Pipe-to-Tee Weld 39-WD-109, dated April 24, 2013 ISI-UT-13-035, UT Calibration/Examination records of 12-Inch Diameter Emergency Condenser  Supply Piping, Tee-to-Pipe Weld 39-WD-110, dated April 24, 2013
ISI-UT-13-036, UT Calibration/Examination Records of 12-Inch Diameter Emergency Condenser
Supply Piping, Pipe-to-Elbow Weld 39-WD-112, dated April 20, 2013
NMP U1 33-WD-046, Phased Array UT Calibration/Examination Records of 6-Inch Diameter  RBCLC Pipe-to-Pipe DM Weld, dated April 29, 2013 UT Calibration/Examination Records of Unit 1 32-WD-042, N2A Safe End-Nozzle DM Weld,
Phased Array Ultrasonic Examination Record, dated April 30, 2013
UT Calibration/Examination Records of Unit 1 32-WD-042, N2A Safe End-to-Nozzle DM Weld
on Recirc Discharge, Phased Array Ultrasonic Examination Record, dated April 30, 2013 UT Calibration/Examination Records of Unit 1 32-WD-082, N2B Safe End-to-Nozzle DM Weld  on Recirc Discharge, Phased Array Ultrasonic Examination Record, dated April 30, 2013 
Attachment
A-6UT Calibration/Examination Records of Uni5 1 32-WD-122, N2C Safe End-to-Nozzle DM Weld on Recirc Discharge, Phased Array Ultrasonic Examination Record, dated April 30, 2013  
UT Calibration/Examination Records of Unit 1 32-WD-164, N2D Safe End-to-Nozzle DM Weld  
on Recirc Discharge, Phased Array Ultrasonic Examination Record, dated April 30, 2013  
UT Calibration/Examination Records of Unit 1 32-WD-208, N2E Safe End-to-Nozzle DM Weld on Recirc Discharge, Phased Array Ultrasonic Examination Record, dated April 30, 2013  
Miscellaneous
Miscellaneous
Audit Report SPC-12-01-N, Special Processes, Testing, & Inspection, dated November 28, 2012  
Audit Report SPC-12-01-N, Special Processes, Testing, & Inspection, dated November 28, 2012
ASME, 2004 Edition  
ASME, 2004 Edition
Section 1R11: Licensed Operator Requa
Section 1R11: Licensed Operator Requalification Program and Licensed Operator
lification Program and Licensed Operator Performance
Performance
  Procedure CNG-OP-1.01-1000, Conduct of Operations, Revision 00900  
Procedure
CNG-OP-1.01-1000, Conduct of Operations, Revision 00900
Condition Reports
Condition Reports
CR-2013-002697 CR-2013-002698 CR-2013-002647 CR-2013-002652  
CR-2013-002697
Section 1R12: Maintenance Effectiveness
CR-2013-002698
  Procedures
CR-2013-002647
CNG-AM-1.01-1023, Maintenance Rule Program, Revision 00201 N2-OP-33, High Pressure Core Spray System, Revision 01201 N2-OSP-CSH-Q@002, HPCS Pump and Valve Operability and System Integrity Test,
CR-2013-002652
Revision 00500
Section 1R12: Maintenance Effectiveness
  Condition Reports
Procedures
CR-2011-006564 CR-2011-006930 CR-2011-007084 CR-2011-007313 CR-2011-007654 CR-2011-007830 CR-2011-009790 CR-2011-010817
CNG-AM-1.01-1023, Maintenance Rule Program, Revision 00201
CR-2012-000359 CR-2012-001459 CR-2012-001614 CR-2012-002176 CR-2012-002198 CR-2012-002249 CR-2012-002711 CR-2012-005017 CR-2012-005119 CR-2012-005999 CR-2012-006141
N2-OP-33, High Pressure Core Spray System, Revision 01201
CR-2012-007193 CR-2012-008548 CR-2012-008816 CR-2012-009400 CR-2012-009982 CR-2012-010499 CR-2013-000159 CR-2013-000563 CR-2013-001491 CR-2013-001633 CR-2013-002768
N2-OSP-CSH-Q@002, HPCS Pump and Valve Operability and System Integrity Test,
CR-2013-002945 CR-2013-002969
      Revision 00500
Miscellaneous
Condition Reports
ACE for CR-2011-006930
CR-2011-006564                   CR-2012-002176                    CR-2012-009400
Attachment  
CR-2011-006930                  CR-2012-002198                    CR-2012-009982
A-7 ACE for CR-2012-002176 Eval-NMP-PRM-03046, (a)(1) Evaluation for 1-PRM-F01
CR-2011-007084                  CR-2012-002249                    CR-2012-010499
CR-2011-007313                  CR-2012-002711                    CR-2013-000159
CR-2011-007654                  CR-2012-005017                    CR-2013-000563
CR-2011-007830                  CR-2012-005119                     CR-2013-001491
CR-2011-009790                  CR-2012-005999                    CR-2013-001633
CR-2011-010817                  CR-2012-006141                    CR-2013-002768
CR-2012-000359                  CR-2012-007193                    CR-2013-002945
CR-2012-001459                  CR-2012-008548                    CR-2013-002969
CR-2012-001614                  CR-2012-008816
Miscellaneous
ACE for CR-2011-006930
                                                                                  Attachment


Unit 1 Containment Spray System Health Report, 1
                                              A-7
st Quarter 2013  
ACE for CR-2012-002176
Unit 1 Neutron Monitoring System Health Report, 1
Eval-NMP-PRM-03046, (a)(1) Evaluation for 1-PRM-F01
st Quarter 2013 Unit 1 Service Water System Health Report, 1
Unit 1 Containment Spray System Health Report, 1st Quarter 2013
st Quarter 2013  
Unit 1 Neutron Monitoring System Health Report, 1st Quarter 2013
Unit 2 High-Pressure Core Spray System Health Report, 1
Unit 1 Service Water System Health Report, 1st Quarter 2013
st Quarter 2013  
Unit 2 High-Pressure Core Spray System Health Report, 1st Quarter 2013
Section 1R13: Maintenance Risk Assessments and Emergent Work Control
Section 1R13: Maintenance Risk Assessments and Emergent Work Control
 
Procedures
Procedures
CNG-MN-4.01-1004, On-Line T-Week Process, Revision 00302  
CNG-MN-4.01-1004, On-Line T-Week Process, Revision 00302
N2-ISP-LDS-Q010, Reactor Building General  
N2-ISP-LDS-Q010, Reactor Building General Area Temperature Instrument Channel Functional
Area Temperature Instrument Channel Functional  
        Test, Revision 00102
Test, Revision 00102 N2-OP-71D, Uninterruptible Power Supplies, Revision 00800 N2-SOP-29.1, Reactor Recirculation Pump Seal Failure, Revision 00101
N2-OP-71D, Uninterruptible Power Supplies, Revision 00800
N2-SOP-97, Reactor Protection Systems Failures, Revision 00401  
N2-SOP-29.1, Reactor Recirculation Pump Seal Failure, Revision 00101
NIP-OUT-01, Shutdown Safety, Revision 03700  
N2-SOP-97, Reactor Protection Systems Failures, Revision 00401
S-ODP-OPS-0122, Posting and Control of Protected Equipment during Online and Outage
NIP-OUT-01, Shutdown Safety, Revision 03700
Operations, Revision 00500  
S-ODP-OPS-0122, Posting and Control of Protected Equipment during Online and Outage
Condition Reports
        Operations, Revision 00500
CR-2013-002461 CR-2013-002916 CR-2013-002926  
Condition Reports
CR-2013-002958  
CR-2013-002461
CR-2013-002998 CR-2013-005021 CR-2013-005077  
CR-2013-002916
Work Orders
CR-2013-002926
WO C90962110 WO C91488068  
CR-2013-002958
WO C90648733  
CR-2013-002998
CR-2013-005021
CR-2013-005077
Work Orders
WO C90962110
WO C91488068
WO C90648733
Miscellaneous
Control Room Operator Logs for Tuesday April 16, 2013
NIP-OUT-01, Shutdown Safety, Revision 03700, Attachment 1, Shutdown Safety Contingency
        Plan (or Equivalent), Contingency Plan No. N1R22-003
NIP-OUT-01, Shutdown Safety, Revision 03700, Attachment 1, Shutdown Safety Contingency
        Plan (or Equivalent), Contingency Plan No. N1R22-004
NIP-OUT-01, Shutdown Safety, Revision 03700, Attachment 1, Shutdown Safety Contingency
        Plan (or Equivalent), Contingency Plan No. N1R22-005
Outage Control Center Logs for Tuesday April 16, 2013
Work Control Center Turnover Sheet for April 16, 2013, Days to Night.
Section 1R15: Operability Determinations and Functionality Assessments
Procedures
CNG-OP-1.01-1002, Conduct of Operability Determinations/Functionality Assessments,
                                                                                Attachment


                                              A-8
      Revision 00200
N1-IPM-092-100, SRM Detector Drive Maintenance and Limit Switch Calibration, Revision 00700
N1-OP-18, Service Water System, Revision 02902
N1-OP-38A, Source Range Monitor, Revision 02000
N1-ST-C5, Secondary Containment and Reactor Building Emergency Ventilation System
      Operability Testing, Revision 01600
N1-ST-C6, Source Range Monitor Operability Test, Revision 01100
Condition Reports
CR-2013-002637                    CR-2013-003186                  CR-2013-003698
CR-2013-002945                    CR-2013-003445                  CR-2013-004481
CR-2013-002969                    CR-2013-003504                  CR-2013-005079
CR-2013-002978                    CR-2013-003520                  CR-2013-004807
CR-2013-003107                    CR-2013-003548
CR- 2013-003116                    CR-2013-003567
CR-2013-003124                    CR-2013-003589
Drawing
RX-147741, 10HN-18 Refinery Pump Elevation, Revision 0
Documents
UFSAR Section VI-2.0, Secondary Containment, Revision 15
UFSAR Section VII-3.0, Emergency Ventilation System, Revision 18
UFSAR Section VII-B, Containment Spray System, Revision 18
UFSAR Section XVI-2.0, Containment Spray System, Revision 20
Section 1R18: Plant Modifications
Procedure
N2-EPM-GEN-V786, MOD Actuator and Damper PM, Revision 00700
Condition Reports
CR-2013-002334
CR-2013-002303
Drawing
ECN Number ECP-12-000616-CN-004 LR18047C
Work Order
WO C919733104
Miscellaneous
Miscellaneous
Control Room Operator Logs for Tuesday April 16, 2013 NIP-OUT-01, Shutdown Safety, Revision 03700, Attachment 1, Shutdown Safety Contingency  Plan (or Equivalent), Contingency Plan No. N1R22-003
ECP 12-000616, Installation of Bubble Tight Damper (BV-210-36)
NIP-OUT-01, Shutdown Safety, Revision 03700, Attachment 1, Shutdown Safety Contingency
ECP 13-000167, Installation of Replacement Pump for Unit 1 Service Water Radiation Monitor
Plan (or Equivalent), Contingency Plan No. N1R22-004 NIP-OUT-01, Shutdown Safety, Revision 03700, Attachment 1, Shutdown Safety Contingency
ECP 13-000347, Temporary Change to Plug Hand Wheel Connection for 2HVP*AOD5A
Plan (or Equivalent), Contingency Plan No. N1R22-005 Outage Control Center Logs for Tuesday April 16, 2013
Section 1R19: Post-Maintenance Testing
Work Control Center Turnover Sheet for April 16, 2013, Days to Night.
                                                                                  Attachment


Section 1R15:  Operability Determinations and Functionality Assessments
                                            A-9
 
Procedures
Procedures
CNG-OP-1.01-1002, Conduct of Operability Determinations/Functionality Assessments, 
CNG-MN-4.01-1008, Pre-/Post-Maintenance Testing, Revision 00100
Attachment
N1-FST-FPP-C005, Ventilation/Smoke Purge System, Revision 00400
A-8 Revision 00200 N1-IPM-092-100, SRM Detector Drive Maintenance and Limit Switch Calibration, Revision 00700
S-EPM-GEN-063, MOV Diagnostic Testing, Revision 00700
N1-OP-18, Service Water System, Revision 02902
Condition Reports
N1-OP-38A, Source Range Monitor, Revision 02000
CR-2013-003051
N1-ST-C5, Secondary Containment and Reactor Building Emergency Ventilation System  Operability Testing, Revision 01600 N1-ST-C6, Source Range Monitor Operability Test, Revision 01100
CR-2013-003251
Condition Reports
CR-2013-004003
CR-2013-002637 CR-2013-002945 CR-2013-002969
CR-2013-004052
CR-2013-002978 CR-2013-003107 CR- 2013-003116 CR-2013-003124 CR-2013-003186 CR-2013-003445 CR-2013-003504 CR-2013-003520 CR-2013-003548 CR-2013-003567
CR-2013-004177
CR-2013-003589 CR-2013-003698 CR-2013-004481 CR-2013-005079 CR-2013-004807
CR-2013-004212
Drawing RX-147741, 10HN-18 Refinery Pump Elevation, Revision 0
CR-2013-004253
 
Drawings
Documents UFSAR Section VI-2.0, Secondary Containment, Revision 15 UFSAR Section VII-3.0, Emergency Ventilation System, Revision 18 UFSAR Section VII-B, Containment Spray System, Revision 18 UFSAR Section XVI-2.0, Containment Spray System, Revision 20
C-19410-C, Elementary Wiring Diagram 4.16 kV Emergency Power Boards and Diesel
 
      Generators (102 and 103 Power Circuits), Revision 28, Sheet 1,
Section 1R18:  Plant Modifications
C-22277-C, 4160 Volt Power Board 102 Connection Diagram Unit 2-1, Diesel Generator 102,
  Procedure N2-EPM-GEN-V786, MOD Actuator and Damper PM, Revision 00700
      Revision 09, Sheet 1
Condition Reports
C-19437-C, Elementary Wiring Diagram 600V, Power Board 161B Control Circuits, Revision 25,
CR-2013-002334 CR-2013-002303
      Sheet 2
C-19437-C, Elementary Wiring Diagram 600V, Power Board 161B Control Circuits, Revision 25,
Drawing ECN Number ECP-12-000616-CN-004 LR18047C 
      Sheet 6
 
C-19017-C, Emergency Cooling System P&I Diagram, Revision 55, Sheet 1
Work Order
WO C919733104
Miscellaneous
ECP 12-000616, Installation of Bubble Tight Damper (BV-210-36)  ECP 13-000167, Installation of Replacement Pump
for Unit 1 Service Water Radiation Monitor  ECP 13-000347, Temporary Change to Plug Hand Wheel Connection for 2HVP*AOD5A
Section 1R19:  Post-Maintenance Testing
 
Attachment
A-9 Procedures
CNG-MN-4.01-1008, Pre-/Post-Maintenance Testing, Revision 00100 N1-FST-FPP-C005, Ventilation/Smoke Purge System, Revision 00400 S-EPM-GEN-063, MOV Diagnostic Testing, Revision 00700  
Condition Reports
CR-2013-003051 CR-2013-003251  
CR-2013-004003 CR-2013-004052 CR-2013-004177 CR-2013-004212 CR-2013-004253  
Drawings C-19410-C, Elementary Wiring Diagram 4.16 kV Emergency Power Boards and Diesel
Generators (102 and 103 Power Circuits), Revision 28, Sheet 1,  
C-22277-C, 4160 Volt Power Board 102 Connection Diagram Unit 2-1, Diesel Generator 102, Revision 09, Sheet 1 C-19437-C, Elementary Wiring Diagram 600V, Power Board 161B Control Circuits, Revision 25,
Sheet 2 C-19437-C, Elementary Wiring Diagram 600V, Power Board 161B Control Circuits, Revision 25,
Sheet 6 C-19017-C, Emergency Cooling System P&I Diagram, Revision 55, Sheet 1  
Work Orders
Work Orders
WO C91473955 WO C91474635  
WO C91473955
WO C91973104  
WO C91474635
WO C92264883  
WO C91973104
WO C92279163  
WO C92264883
WO C92279776  
WO C92279163
Miscellaneous
WO C92279776
ECP-13-000420-015-9, Removal and Replacement of Existing Cable 102-33 from EDG102 to Power Board 102, Revision 0000 ECP-12-000575, Standard Spec for Electrical Installation Activities at NMP1, Revision 21.00 N21036, Limitorque Type SMB and SB Instruction and Maintenance Manual, NMPCNO:   N2L20000VALVOP004 SPEC NMP1-325M, Section II, Penetration Seals, Revision 1  
Miscellaneous
Section 1R20: Refueling and Other Outage Activities
ECP-13-000420-015-9, Removal and Replacement of Existing Cable 102-33 from EDG102 to
 
      Power Board 102, Revision 0000
ECP-12-000575, Standard Spec for Electrical Installation Activities at NMP1, Revision 21.00
N21036, Limitorque Type SMB and SB Instruction and Maintenance Manual, NMPCNO:
      N2L20000VALVOP004
SPEC NMP1-325M, Section II, Penetration Seals, Revision 1
Section 1R20: Refueling and Other Outage Activities
Procedures
Procedures
CNG-OP-3.01-1000, Reactivity Management, Revision 00800
CNG-OP-3.01-1000, Reactivity Management, Revision 00800
Attachment  
                                                                                      Attachment
A-10N1-FHP-27C, Core Shuffle, Revision 00603 N1-FHP-25, General Description of Fuel Moves, Revision 02301 N1-OP-43C, Plant Shutdown, Revision 01200 N1-RESP-9, SRM Operability for Core Alterations, Revision 00001 N1-ST-V3, Rod Worth Minimizer Operability Test APRM/IRM Overlap Verification, Revision
 
01300
                                            A-10
N1-FHP-27C, Core Shuffle, Revision 00603
N1-FHP-25, General Description of Fuel Moves, Revision 02301
N1-OP-43C, Plant Shutdown, Revision 01200
N1-RESP-9, SRM Operability for Core Alterations, Revision 00001
N1-ST-V3, Rod Worth Minimizer Operability Test APRM/IRM Overlap Verification, Revision
      01300
Condition Report
Condition Report
CR-2013-002793  
CR-2013-002793
Tagout TO-30-0224  
Tagout
TO-30-0224
Miscellaneous
RFO22 Fuel Movement Instructions
Section 1R22: Surveillance Testing
Procedures
N1-ISP-LRT-TYC, Type C Containment Isolation Valve Local Leak Rate Test, Revision 00900
N1-ST-C5, Secondary Containment and Reactor Building Emergency Ventilation System
      Operability Test, Revision 01600
N1-ST-Q15, Condensate Transfer System Operability Test, Revision 00703
N1-ST-Q3, High-Pressure Coolant Injection Pump and Check Valve Operability Test,
      Revision 01300
N1-TSP-201-001, Integrated Leak Rate Test of Primary Containment Type A Test, Revision
      00600
N2-CSP-GEN-D100, Reactor Water/Auxiliary Water Chemistry Surveillance, Revision 00601
N2-ISP-LDS-Q010, Reactor Building General Area Temperature Instrument Channel Functional
      Test, Revision 00103
N22-CSP-W@101, Weekly Conductivity Monitor Channel Check, Revision 1
S-CAD-CHE-101, Chemistry Sample Conduct, Revision 0100
Condition Reports
CR-2013-002788
CR-2013-002637
Drawings
C-18013-C, Reactor Building Heating and Ventilation System, Revision 33
C-18014-C, Reactor Containment (Drywell and Torus) Inert Gas N2 Purge and Fill Drywell
      Cooling System, Revision 58
Work Orders
WO C91214116
WO C92182070
                                                                                  Attachment


Miscellaneous
                                              A-11
RFO22 Fuel Movement Instructions
Miscellaneous
NUREG-1493, Performance-Based Containment Leak Test Program, September 1995
Section 1EP4: Emergency Action Level and Emergency Plan Changes
Section 1R22:  Surveillance Testing
Procedures
  Procedures
EPIP-EPP-01, Classification of Emergency Conditions at Unit 1, Revision 23
N1-ISP-LRT-TYC, Type 'C' Containment Isolation Valve Local Leak Rate Test, Revision 00900  N1-ST-C5, Secondary Containment and Reactor Building Emergency Ventilation System  Operability Test, Revision 01600  N1-ST-Q15, Condensate Transfer System Operability Test, Revision 00703  N1-ST-Q3, High-Pressure Coolant Injection Pump and Check Valve Operability Test, 
EPIP-EPP-02, Classification of Emergency Conditions at Unit 2, Revision 22
Revision 01300  N1-TSP-201-001, Integrated Leak Rate Test of Primary Containment Type 'A' Test, Revision 
EPMP-EPP-0101, Unit 1 Emergency Classification Technical Bases, Revision 01700
00600 N2-CSP-GEN-D100, Reactor Water/Auxiliary Water Chemistry Surveillance, Revision 00601 N2-ISP-LDS-Q010, Reactor Building General Area Temperature Instrument Channel Functional  Test, Revision 00103 N22-CSP-W@101, Weekly Conductivity Monitor Channel Check, Revision 1 S-CAD-CHE-101, Chemistry Sample Conduct, Revision 0100
EPMP-EPP-0102, Unit 2 Emergency Classification Technical Bases, Revision 01900
Condition Reports
Section 1EP6: Drill Evaluation
CR-2013-002788
Procedure
CR-2013-002637
EPIP-EPP-01, Classification of Emergency Conditions at Unit 1, Revision 02000
Drawings C-18013-C, Reactor Building Heating and Ventilation System, Revision 33 
Section 2RS1: Radiological Hazard Assessment and Exposure Controls
C-18014-C, Reactor Containment (Drywell and Torus) Inert Gas N2 Purge and Fill Drywell 
Procedures
Cooling System, Revision 58 
CNG-TR-1.01-1025, Radiation Protection Technician Training Program, Revision 00100
Work Orders
GAP-RPP-08, Control of High Locked High and Very High Radiation Areas, Revision 16
WO C91214116 WO C92182070 
S-RAP-RPP-0103, Posting and Barricading Radiological Areas, Revision 02800
Attachment
S-RAP-RPP-0201, Radiation Work Permit Initiation, Preparation, Control and Use,
A-11Miscellaneous
        Revision 02300
NUREG-1493, Performance-Based Contai
S-RAP-RPP-0801, High Locked High and Very High Radiation Area Monitoring and Control,
nment Leak Test Program, September 1995  
        Revision 03000
S-RPIP-3.0, Radiological Surveys, Revision 01900
Section 1EP4: Emergency Action Level and Emergency Plan Changes
Condition Reports
  Procedures
CR-2013-002520
EPIP-EPP-01, Classification of Emergency Conditions at Unit 1, Revision 23  
CR-2013-002781
EPIP-EPP-02, Classification of Emergency Conditions at Unit 2, Revision 22 EPMP-EPP-0101, Unit 1 Emergency Classifi
CR-2013-003098
cation Technical Bases, Revision 01700 EPMP-EPP-0102, Unit 2 Emergency Classifi
Audits, Self Assessments, and Surveillances
cation Technical Bases, Revision 01900  
Q&PA Assessment Report 13-010, Assess Station Preparedness for Managing and Executing
Section 1EP6: Drill Evaluation
        N1R23
  Procedure EPIP-EPP-01, Classification of Emergency Conditions at Unit 1, Revision 02000  
SA-2013-000005, Snapshot Assessment of 2012 4th Quarter Dose and Dose Rate Alarms
Section 2RS1: Radiological Hazard Assessment and Exposure Controls
SA-2013-000034, Snapshot Assessment of Radiation Protection Job Hazard Analysis Process
  Procedures
        Usage
CNG-TR-1.01-1025, Radiation Protection Technician Training Program, Revision 00100 GAP-RPP-08, Control of High Locked High and Very High Radiation Areas, Revision 16  
Miscellaneous
S-RAP-RPP-0103, Posting and Barricading Radiological Areas, Revision 02800  
BRAC Survey Trends in Discharge Piping Dose Rates, Unit 1, 1984 to 2013
S-RAP-RPP-0201, Radiation Work Permit Initiation, Preparation, Control and Use,
BRAC Survey Trends in Recirc Suction Piping Dose Rates, Unit 1, 1984 to 2013
Revision 02300 S-RAP-RPP-0801, High Locked High and Very High Radiation Area Monitoring and Control,   Revision 03000 S-RPIP-3.0, Radiological Surveys, Revision 01900  
High Radiation Area/Locked High Radiation Area Gate Door Checklist, Unit 1, April 20, 2013
Personnel Qualification Form Verification, Employee Badge 38016, April 8, 2013
Personnel Qualification Form Verification, Employee Badge 38359, April 1, 2013
Personnel Qualification Form Verification, Employee Badge 4127, April 8, 2013
Personnel Qualification Form Verification, Employee Badge 4169, April 1, 2013
Personnel Qualification Form Verification, Employee Badge 4196, March 29, 2013
                                                                                    Attachment


                                              A-12
Personnel Qualification Form Verification, Employee Badge 54337, February 25, 2013
RWP 113330H, RB 261 Reactor Water Cleanup Valve Work
RWP 113802H, Drywell Under-Vessel Work
RWP 113806H, Drywell In-Service Inspection
RWP 113810, Drywell General Scaffolding Activities
RWP 113815, RB 261 FAC In-Service Inspection
RWP 113890A, RB 340 Reactor Disassembly and Reassembly
RWP 113890B, RB 340 Underwater Work on Refuel Floor
RWP 113890E, RB 340 Reactor Cavity and Equipment Storage Pit Decon
RWP 113891, Spent Fuel Pool Gate Repair
Section 2RS2: Occupational ALARA Planning and Controls
Procedures
CNG-RP-1.01-1001, Station ALARA Committee, Revision 00000
CNG-RP-1.01-2003, Operational ALARA Planning and Controls, Revision 00000
N1-OP-34, Refueling Procedure (Includes Primary Chemistry Controls), Revision 03000
S-RAP-ALA-0101, Temporary Shielding, Revision 10
S-RAP-ALA-0102, ALARA Reviews, Revision 01500
Condition Reports
Condition Reports
CR-2013-002520  CR-2013-002781 CR-2013-003098
CR-2013-002267
 
CR-2013-003168
Audits, Self Assessments, and Surveillances
Self Assessment
Q&PA Assessment Report 13-010, Assess Station Preparedness for Managing and Executing  N1R23
SA-2012-000283, 4th Quarter 2012 ALARA Committee Effectiveness Review
SA-2013-000005, Snapshot Assessment of 2012 4
th Quarter Dose and Dose Rate Alarms SA-2013-000034, Snapshot Assessment of Radiation Protection Job Hazard Analysis Process
Usage
Miscellaneous
BRAC Survey Trends in Discharge Piping Dose Rates, Unit 1, 1984 to 2013 BRAC Survey Trends in Recirc Suction Piping Dose Rates, Unit 1, 1984 to 2013 High Radiation Area/Locked High Radiation Area Gate Door Checklist, Unit 1, April 20, 2013
Personnel Qualification Form Verification, Employee Badge 38016, April 8, 2013
Personnel Qualification Form Verification, Employee Badge 38359, April 1, 2013
Personnel Qualification Form Verification, Employee Badge 4127, April 8, 2013
Personnel Qualification Form Verification, Employee Badge 4169, April 1, 2013 Personnel Qualification Form Verification, Employee Badge 4196, March 29, 2013 
Attachment
A-12Personnel Qualification Form Verification, Employee Badge 54337, February 25, 2013 RWP 113330H, RB 261 Reactor Water Cleanup Valve Work
 
RWP 113802H, Drywell Under-Vessel Work
RWP 113806H, Drywell In-Service Inspection
RWP 113810, Drywell General Scaffolding Activities RWP 113815, RB 261 FAC In-Service Inspection RWP 113890A, RB 340 Reactor Disassembly and Reassembly
RWP 113890B, RB 340 Underwater Work on Refuel Floor
RWP 113890E, RB 340 Reactor Cavity and Equipment Storage Pit Decon
 
RWP 113891, Spent Fuel Pool Gate Repair
Section 2RS2:  Occupational ALARA Planning and Controls
  Procedures
CNG-RP-1.01-1001, Station ALARA Committee, Revision 00000
CNG-RP-1.01-2003, Operational ALARA Planning and Controls, Revision 00000 N1-OP-34, Refueling Procedure (Includes Primary Chemistry Controls), Revision 03000
S-RAP-ALA-0101, Temporary Shielding, Revision 10
S-RAP-ALA-0102, ALARA Reviews, Revision 01500
Condition Reports
CR-2013-002267
CR-2013-003168  
Self Assessment
SA-2012-000283, 4
th Quarter 2012 ALARA Committee Effectiveness Review  
Miscellaneous
Miscellaneous
5-Year Collective Radiation Exposure Reduction Plan, 2012 to 2016 ALARA Plan 2013-1-002, Drywell Under-Vessel Activities and Associated Activities N1R22, April 10, 2013 ALARA Plan 2013-1-004, Drywell Operations and LLRT/ILRT Activities, April 10, 2013  
5-Year Collective Radiation Exposure Reduction Plan, 2012 to 2016
ALARA Plan 2013-1-006, Drywell ISI Activities, April 10, 2013 ALARA Plan 2013-1-007, Recirc Pump Seals Replacement and Motor PMs (Numbers 11, 13 and 15), April 10, 2013 ALARA Plan 2013-1-010, Drywell Scaffold Activities, April 10, 2013  
ALARA Plan 2013-1-002, Drywell Under-Vessel Activities and Associated Activities N1R22,
ALARA Plan 2013-1-014, Drywell Emergency Relief  
      April 10, 2013
Valve and Pilot Valve Work Activities, April 10, 2013 ALARA Plan 2013-1-024, Main Steam Isolation Valve 01-02 Stem Replacement Actuator Remove/Replace and Testing, April 10, 2013 ALARA Plan 2013-1-029, Balance of Plant FAC Activities in RWCU HX Room and Valve Aisles, April 10, 2013 ALARA Plan 2013-1-030, Refuel Floor Activities, dated April 10, 2013  
ALARA Plan 2013-1-004, Drywell Operations and LLRT/ILRT Activities, April 10, 2013
ALARA Plan 2013-1-031, RWCU Miscellaneous Maintenance, PM, ST, Operations RFO 22, April 10, 2013 ALARA Work In-Progress Review, 2013-1-006, Drywell ISI Activities, April 21, 2013  
ALARA Plan 2013-1-006, Drywell ISI Activities, April 10, 2013
ALARA Work In-Progress Review, 2013-1-007, Recirc Pump Seals Replacement and Motor PMs, April 22, 2013 ALARA Work In-Progress Review, 2013-1-010, Drywell Scaffold Activities, April 20, 2013
ALARA Plan 2013-1-007, Recirc Pump Seals Replacement and Motor PMs (Numbers 11, 13 and
Attachment  
      15), April 10, 2013
A-13ALARA Work In-Progress Review, 2013-1-011, Drywell Insulation, April 22, 2013 ALARA Work In-Progress Review, 2013-1-014, Drywell Emergency Relief Valve and Pilot Valve Work Activities, April 22, 2013 ALARA Work In-Progress Review, 2013-1-024, Main Steam Isolation Valve 01-02 Stem Replacement Actuator Remove/Replace and Testing, April 22, 2013 ALARA Work In-Progress Review, 2013-1-029, Balance of Plant FAC Activities in RWCU HX Room and Valve Aisles, April 18, 2013 ALARA Work In-Progress Review, 2013-1-030, Refuel Floor Activities, April 20, 2013
ALARA Plan 2013-1-010, Drywell Scaffold Activities, April 10, 2013
Unit 1 Radiation Protection Pre-Outage Report, dated April 15, 2013
ALARA Plan 2013-1-014, Drywell Emergency Relief Valve and Pilot Valve Work Activities,
      April 10, 2013
ALARA Plan 2013-1-024, Main Steam Isolation Valve 01-02 Stem Replacement Actuator
      Remove/Replace and Testing, April 10, 2013
ALARA Plan 2013-1-029, Balance of Plant FAC Activities in RWCU HX Room and Valve Aisles,
      April 10, 2013
ALARA Plan 2013-1-030, Refuel Floor Activities, dated April 10, 2013
ALARA Plan 2013-1-031, RWCU Miscellaneous Maintenance, PM, ST, Operations RFO 22,
      April 10, 2013
ALARA Work In-Progress Review, 2013-1-006, Drywell ISI Activities, April 21, 2013
ALARA Work In-Progress Review, 2013-1-007, Recirc Pump Seals Replacement and Motor PMs,
      April 22, 2013
ALARA Work In-Progress Review, 2013-1-010, Drywell Scaffold Activities, April 20, 2013
                                                                                    Attachment


                                              A-13
Section 2RS3: In-Plant Airborne Radioactivity Control and Mitigation
ALARA Work In-Progress Review, 2013-1-011, Drywell Insulation, April 22, 2013
  Procedures
ALARA Work In-Progress Review, 2013-1-014, Drywell Emergency Relief Valve and Pilot Valve
GAP-RPP-04, Respiratory Protection Program, Revision 11  
        Work Activities, April 22, 2013
N1-RTP-76, Operation and Calibration of the Eberline PING-1A PING-1AMT Particulate Iodine Noble Gas Monitor, Revision 02 S-RAP-RPP-0402, Selection and Issuance of Radiological Respiratory Protection Equipment,   Revision 12  
ALARA Work In-Progress Review, 2013-1-024, Main Steam Isolation Valve 01-02 Stem
S-RPIP-4.2, Respiratory Protection Quality Assurance Control Program, Revision 00200  
        Replacement Actuator Remove/Replace and Testing, April 22, 2013
S-RPIP-4.4, Maintenance Inspection and Testing of Respiratory Protection Equipment,  
ALARA Work In-Progress Review, 2013-1-029, Balance of Plant FAC Activities in RWCU HX
Revision 00700 S-RPIP-4.5, Use of Respiratory Protection Equipment, Revision 09 S-RPIP-6.0, Control and Use of HEPA Vacuum Cleaners and Portable HEPA Ventilation Units, Revision 00300  
        Room and Valve Aisles, April 18, 2013
ALARA Work In-Progress Review, 2013-1-030, Refuel Floor Activities, April 20, 2013
Unit 1 Radiation Protection Pre-Outage Report, dated April 15, 2013
Section 2RS3: In-Plant Airborne Radioactivity Control and Mitigation
Procedures
GAP-RPP-04, Respiratory Protection Program, Revision 11
N1-RTP-76, Operation and Calibration of the Eberline PING-1A PING-1AMT Particulate Iodine
        Noble Gas Monitor, Revision 02
S-RAP-RPP-0402, Selection and Issuance of Radiological Respiratory Protection Equipment,
        Revision 12
S-RPIP-4.2, Respiratory Protection Quality Assurance Control Program, Revision 00200
S-RPIP-4.4, Maintenance Inspection and Testing of Respiratory Protection Equipment,
        Revision 00700
S-RPIP-4.5, Use of Respiratory Protection Equipment, Revision 09
S-RPIP-6.0, Control and Use of HEPA Vacuum Cleaners and Portable HEPA Ventilation Units,
        Revision 00300
Condition Reports
Condition Reports
CR-2013-002816 CR-2013-002947  
CR-2013-002816
CR-2013-002947
Self Assessment
Self Assessment
SA-2011-000164, Radiological Respiratory Protection Program, November 18, 2011  
SA-2011-000164, Radiological Respiratory Protection Program, November 18, 2011
Miscellaneous
Air Sample Unit 1 RB 340 Edge of Cavity, April 15, 2013, 5:43 a.m.
Air Sample Unit 1 RB 340 Edge of Cavity, April 15, 2013, 7:14 a.m.
Air Sample Unit 1 RB 340 Refuel Floor during Silver Dollar Installation, April 15, 2013, 9:20 p.m.
Air Sample Unit 1 RB 340 Refuel Floor during Stud Removal, April 17, 2013, 12:20 p.m.
HEPA Ventilation Log, dated April 23, 2013
Unit 1 System Health Report for 1st Quarter Control Room Ventilation, dated April 10, 2013
Unit 1 System Health Report for 1st Quarter RB Ventilation, dated April 10, 2013
Vacuum Cleaner Issue Log, dated April 23, 2013
Section 2RS4: Occupational Dose Assessment
Procedures
CNG-RP-1.01-2002 Effective Dose Equivalent - External, Revision 00000
CNG-RP-1.01-3002, Sampling and Analysis for 10 CFR 61 Waste Classification, Revision 00000
GAP-RPP-07, Internal and External Dosimetry Program, Revision 02100
S-RAP-ALA-0103, Dosimetry and Radiological Engineering Evaluations, Revision 00900
S-RPIP-4.6, DAC Hour Tracking and Estimating Internal Exposure, Revision 00500
                                                                                        Attachment


Miscellaneous
                                            A-14
Air Sample Unit 1 RB 340 Edge of Cavity, April 15, 2013, 5:43 a.m. 
S-RPIP-5.5, Processing and Evaluating Personnel Contamination, Revision 01800
Air Sample Unit 1 RB 340 Edge of Cavity, April 15, 2013, 7:14 a.m.
S-RPIP-5.7, Bioassay and Internal Dose Assessment, Revision 00900
Air Sample Unit 1 RB 340 Refuel Floor during Silver Dollar Installation, April 15, 2013, 9:20 p.m.
S-RPIP-5.20, Dosimetry Program Quality Assurance, Revision 00800
Air Sample Unit 1 RB 340 Refuel Floor during Stud Removal, April 17, 2013, 12:20 p.m.
S-RPIP-5.25, Exposure Evaluation Reports, Revision 01000
HEPA Ventilation Log, dated April 23, 2013 Unit 1 System Health Report for 1
Condition Reports
st Quarter Control Room Ventilation, dated April 10, 2013 Unit 1 System Health Report for 1
CR-2013-002474
st Quarter RB Ventilation, dated April 10, 2013 Vacuum Cleaner Issue Log, dated April 23, 2013
CR-2013-002678
 
CR-2013-002974
Section 2RS4:  Occupational Dose Assessment
CR-2013-003247
  Procedures
CR-2013-003374
CNG-RP-1.01-2002 Effective Dose Equivalent - External, Revision 00000
CR-2013-003350
CNG-RP-1.01-3002, Sampling and Analysis for 10 CFR 61 Waste Classification, Revision 00000
GAP-RPP-07, Internal and External Dosimetry Program, Revision 02100 S-RAP-ALA-0103, Dosimetry and Radiological Engineering Evaluations, Revision 00900 S-RPIP-4.6, DAC Hour Tracking and Estimating Internal Exposure, Revision 00500 
Attachment
A-14S-RPIP-5.5, Processing and Evaluating Personnel Contamination, Revision 01800 S-RPIP-5.7, Bioassay and Internal Dose Assessment, Revision 00900  
S-RPIP-5.20, Dosimetry Program Quality Assurance, Revision 00800  
S-RPIP-5.25, Exposure Evaluation Reports, Revision 01000  
 
Condition Reports
CR-2013-002474  
CR-2013-002678  
CR-2013-002974  
CR-2013-003247 CR-2013-003374 CR-2013-003350  
CR-2013-003413
CR-2013-003413
 
Miscellaneous
Miscellaneous
Oak Ridge Associated University E-mail Y. McCormick to A. Moisan RE: REIRS Data Verification, dated April 1, 2013 Sentinel Report on Personnel with Dose Greater Than 400 mrem, dated April 22, 2013  
Oak Ridge Associated University E-mail Y. McCormick to A. Moisan RE: REIRS Data Verification,
S-RPIP-5.5 Attachment 1 Contamination Occurrence Report Number 1-13-RFO-003, dated April 24, 2013  
      dated April 1, 2013
Sentinel Report on Personnel with Dose Greater Than 400 mrem, dated April 22, 2013
Section 2RS7: Radiological Environmental Monitoring Program
S-RPIP-5.5 Attachment 1 Contamination Occurrence Report Number 1-13-RFO-003, dated
  Procedures
      April 24, 2013
CNG-EV-1.01-1000, Radiological Environmental Monitoring Program, Revision 001000  
Section 2RS7: Radiological Environmental Monitoring Program
NLAP-ENV-400, Radiological Environmental Monitoring Program Land Use Census, Inter-laboratory Comparison Program and Reporting, Revision 00.00 S-ENVSP-3, Radiological Sample Collection, Processing, and Shipment Land Use Census Quality Control (Vendor Procedure), Revision 06.00  
Procedures
S-ENVSP-3.1, Milk Animal Census and Milk Sample Collection, Revision 01.00  
CNG-EV-1.01-1000, Radiological Environmental Monitoring Program, Revision 001000
S-ENVSP-3.2, Garden/Irrigation Census and Food Product (Vegetation and Irrigation Crop) Sample Collection, Revision 02.00 S-ENVSP-3.3, Nearest Meat Animal Census and Meat, Poultry, and Egg Sample Collection, Revision 01.00  
NLAP-ENV-400, Radiological Environmental Monitoring Program Land Use Census,
S-ENVSP-3.4, Soil Sample Collection, Revision 01.00  
      Inter-laboratory Comparison Program and Reporting, Revision 00.00
S-ENVSP-3.5, Fish Sample Collection, Revision 01.00  
S-ENVSP-3, Radiological Sample Collection, Processing, and Shipment Land Use Census
S-ENVSP-3.6, Shoreline Sediment and Cladophora Sample Collection, Revision 01.00  
      Quality Control (Vendor Procedure), Revision 06.00
S-ENVSP-3.7, Nearest Residence Census, Revision 00.00 S-ENVSP-4.1, TLD/OSL Preparation, Collection and Analysis, Revision 01400.00 S-ENVSP-4.2, Environmental Air Monitoring Sample Collection, Revision 01001.00  
S-ENVSP-3.1, Milk Animal Census and Milk Sample Collection, Revision 01.00
S-ENVSP-4.3, Environmental Air Monitoring Station Inspection and Maintenance,
S-ENVSP-3.2, Garden/Irrigation Census and Food Product (Vegetation and Irrigation Crop)
Revision 00600.00 S-ENVSP-4.4, Environmental Surface Water Sample Collection and Compositing,
      Sample Collection, Revision 02.00
Revision 00900.00 S-ENVSP-12, Environmental Surveillance Quality Assurance/Quality Control Program,
S-ENVSP-3.3, Nearest Meat Animal Census and Meat, Poultry, and Egg Sample Collection,
Revision 001100.00 S-ENVSP-15, Sampling and Analysis for Unmonitored Pathways, Revision 01300.00  
      Revision 01.00
S-ENVSP-16, Sampling and Analysis of Monitoring Wells, Revision 00500.00 S-ENVSP-18, Environmental Data Review, Revision 01000.00 S-IPM-MET-001, Meteorological Monitoring System Equipment Check, Revision 00200.00
S-ENVSP-3.4, Soil Sample Collection, Revision 01.00
Attachment  
S-ENVSP-3.5, Fish Sample Collection, Revision 01.00
A-15 S-IPM-MET-201, Dew Point Calibration, Revision 00100.00 S-IPM-MET-301, Barometric Pressure Calibration, Revision 03.00
S-ENVSP-3.6, Shoreline Sediment and Cladophora Sample Collection, Revision 01.00
S-IPM-MET-401, Precipitation Gauge Calibration, Revision 02.00
S-ENVSP-3.7, Nearest Residence Census, Revision 00.00
S-IPM-MET-601, Main Meteorological Tower 30 Foot Wind Speed and Direction Calibration,
S-ENVSP-4.1, TLD/OSL Preparation, Collection and Analysis, Revision 01400.00
Revision 00100.00 S-IPM-MET-602, Main Meteorological Tower 100 Foot Wind Speed and Direction Calibration,  Revision 00400.00
S-ENVSP-4.2, Environmental Air Monitoring Sample Collection, Revision 01001.00
S-IPM-MET-603, Main Meteorological Tower 200 Foot Wind Speed and Direction Calibration,
S-ENVSP-4.3, Environmental Air Monitoring Station Inspection and Maintenance,
Revision 00100.00
      Revision 00600.00
S-IPM-MET-611, Backup Meteorological Tower Wind Speed and Direction Calibration, 
S-ENVSP-4.4, Environmental Surface Water Sample Collection and Compositing,
Revision 00200.00 S-IPM-MET-621, Inland Meteorological Tower Wind Speed and Direction Calibration, 
      Revision 00900.00
Revision 00100.00 S-IPM-MET-701, Temperature and Delta Temperature Instrument Calibration, 
S-ENVSP-12, Environmental Surveillance Quality Assurance/Quality Control Program,
Revision 00200.00 S-MET-ENV-01, Maintenance of Meteorological Monitoring Program, Revision 00100.00 S-MET-ENV-0002, Meteorological Data Verification and Edit, Revision 00600.00 S-MET-ENV-0003, Meteorological Monitoring Program Quality Assurance Quality Control, 
      Revision 001100.00
Revision 00600.00
S-ENVSP-15, Sampling and Analysis for Unmonitored Pathways, Revision 01300.00
S-ENVSP-16, Sampling and Analysis of Monitoring Wells, Revision 00500.00
S-ENVSP-18, Environmental Data Review, Revision 01000.00
S-IPM-MET-001, Meteorological Monitoring System Equipment Check, Revision 00200.00
                                                                                  Attachment


                                              A-15
S-IPM-MET-201, Dew Point Calibration, Revision 00100.00
S-IPM-MET-301, Barometric Pressure Calibration, Revision 03.00
S-IPM-MET-401, Precipitation Gauge Calibration, Revision 02.00
S-IPM-MET-601, Main Meteorological Tower 30 Foot Wind Speed and Direction Calibration,
        Revision 00100.00
S-IPM-MET-602, Main Meteorological Tower 100 Foot Wind Speed and Direction Calibration,
        Revision 00400.00
S-IPM-MET-603, Main Meteorological Tower 200 Foot Wind Speed and Direction Calibration,
        Revision 00100.00
S-IPM-MET-611, Backup Meteorological Tower Wind Speed and Direction Calibration,
        Revision 00200.00
S-IPM-MET-621, Inland Meteorological Tower Wind Speed and Direction Calibration,
        Revision 00100.00
S-IPM-MET-701, Temperature and Delta Temperature Instrument Calibration,
        Revision 00200.00
S-MET-ENV-01, Maintenance of Meteorological Monitoring Program, Revision 00100.00
S-MET-ENV-0002, Meteorological Data Verification and Edit, Revision 00600.00
S-MET-ENV-0003, Meteorological Monitoring Program Quality Assurance Quality Control,
        Revision 00600.00
Condition Reports
Condition Reports
CR-2012-000632 CR-2012-000664
CR-2012-000632                   CR-2012-005817                    CR-2012-010132
CR-2012-000734
CR-2012-000664                    CR-2012-006057                    CR-2013-000603
CR-2012-001143
CR-2012-000734                    CR-2012-007114                   CR-2013-001001
CR-2012-001488 CR-2012-005817 CR-2012-006057
CR-2012-001143                    CR-2012-007684
CR-2012-007114  
CR-2012-001488                    CR-2012-009863
CR-2012-007684
Work Orders
CR-2012-009863 CR-2012-010132 CR-2013-000603
WO C91660878
CR-2013-001001
WO C91875097
Work Orders
WO C91660878  
WO C91875097  
 
Audits, Self Assessments, and Surveillances
Audits, Self Assessments, and Surveillances
DTE Energy NAQA-12-0036, Audit 12-006 of Environmental Dosimetry Company, July 3, 2012  
DTE Energy NAQA-12-0036, Audit 12-006 of Environmental Dosimetry Company, July 3, 2012
Entergy CR-LO-JAFLO-2012-00045, Radiological Environmental Monitoring Program Focused
Entergy CR-LO-JAFLO-2012-00045, Radiological Environmental Monitoring Program Focused
Self Assessment, February 20 to 27, 2013 NUPIC Audit 22873, GEL Laboratories, LLC, Analytical Laboratory Services, December 13, 2011  
        Self Assessment, February 20 to 27, 2013
NUPIC Audit 22873, GEL Laboratories, LLC, Analytical Laboratory Services, December 13, 2011
Miscellaneous
Miscellaneous
2011 Annual Report, Meteorological Monitoring Program, Murray and Trettel, Inc., Palatine, IL  
2011 Annual Report, Meteorological Monitoring Program, Murray and Trettel, Inc., Palatine, IL
2012 Annual Quality Assurance Status Report, Environmental Dosimetry Company, dated
2012 Annual Quality Assurance Status Report, Environmental Dosimetry Company, dated
March 13, 2013 2012 Inter-laboratory Comparison Report, Eckert and Zeigler, dated March 29, 2013 2012 Land Use Census Summary Report, dated October 25, 2012  
        March 13, 2013
DVP-04.01, Environmental Laboratory Quality Assurance/Quality Control Program, Revision 4  
2012 Inter-laboratory Comparison Report, Eckert and Zeigler, dated March 29, 2013
EN-CY-102, Laboratory Analytical Quality Control, Revision 4  
2012 Land Use Census Summary Report, dated October 25, 2012
DVP-04.01, Environmental Laboratory Quality Assurance/Quality Control Program, Revision 4
EN-CY-102, Laboratory Analytical Quality Control, Revision 4
James A. FitzPatrick Environmental Laboratory Quality Assurance Report, January to
        December 2011
Licensee Event Number 48901, Power Lost to Meteorological Instrumentation, dated April 9, 2013
Quality Assurance Topical Report, dated December 11, 2011
                                                                                    Attachment


James A. FitzPatrick Environmental Laboratory Quality Assurance Report, January to  December 2011 Licensee Event Number 48901, Power Lost to Meteorological Instrumentation, dated April 9, 2013
                                              A-16
Quality Assurance Topical Report, dated December 11, 2011 
Radiological Environmental Operating Report January to December, 2012, dated May 15, 2013
Attachment
Radiological Engineering Evaluation Number C-99-011, Revision 7, 10 CFR 50.75(g) Record -
A-16Radiological Environmental Operating Report January to December, 2012, dated May 15, 2013 Radiological Engineering Evaluation Number C-99-011, Revision 7, 10 CFR 50.75(g) Record -  
        Unit 1 TB Roof Replacement, dated September 7, 2012
Unit 1 TB Roof Replacement, dated September 7, 2012  
Radiological Engineering Evaluation Number C-99-011, Revision 8, 10 CFR 50.75(g) Record -
Radiological Engineering Evaluation Number C-99-011, Revision 8, 10 CFR 50.75(g) Record -  
        Elevated Tritium Concentration in Screen House In-Leakage, dated January 27, 2013
Elevated Tritium Concentration in Screen House In-Leakage, dated January 27, 2013 S-ENVSP-4.4 Attachment 5A L/S 7523 Sample Pump Control Setting Determination, Serial Number L03004172, NRG Oswego Steam Station, dated August 14, 2009  
S-ENVSP-4.4 Attachment 5A L/S 7523 Sample Pump Control Setting Determination, Serial
S-ENVSP-4.4, Attachment 5A, L/S 7523 Sample Pump Control Setting Determination, Serial  
        Number L03004172, NRG Oswego Steam Station, dated August 14, 2009
Number L04004587, Unit 1 Intake Canal, dated April 20, 2009  
S-ENVSP-4.4, Attachment 5A, L/S 7523 Sample Pump Control Setting Determination, Serial
S-ENVSP-4.4, Attachment 5A, L/S 7523 Sample Pump Control Setting Determination, Serial Number L04004590, Unit 1 Intake Canal, dated April 20, 2009 Tektronix Certificate of Calibration 6776890, American Meter Mass Flow Meter Number 10429,  
        Number L04004587, Unit 1 Intake Canal, dated April 20, 2009
dated November 16, 2012  
S-ENVSP-4.4, Attachment 5A, L/S 7523 Sample Pump Control Setting Determination, Serial
Tektronix Certificate of Calibration 6104009, American Meter Mass Flow Meter Number 10436,  
        Number L04004590, Unit 1 Intake Canal, dated April 20, 2009
dated April 20, 2012  
Tektronix Certificate of Calibration 6776890, American Meter Mass Flow Meter Number 10429,
Tektronix Certificate of Calibration 6780305, American Meter Mass Flow Meter Number 10458, dated November 17, 2012 Tektronix Certificate of Calibration 6114558, American Meter Mass Flow Meter Number 10870,  
        dated November 16, 2012
dated April 23, 2012  
Tektronix Certificate of Calibration 6104009, American Meter Mass Flow Meter Number 10436,
Tektronix Certificate of Calibration 6380789, American Meter Mass Flow Meter Number 10899,  
        dated April 20, 2012
dated July 18, 2012 Unit 1 ODCM, Revision 34 Unit 1 Radioactive Effluent Release Report, January to December 2012, dated May 1, 2013  
Tektronix Certificate of Calibration 6780305, American Meter Mass Flow Meter Number 10458,
Unit 2 ODCM, Revision 35  
        dated November 17, 2012
Unit 2 UFSAR Chapter 2.3, Meteorology, Revision 19, October 2010  
Tektronix Certificate of Calibration 6114558, American Meter Mass Flow Meter Number 10870,
        dated April 23, 2012
Tektronix Certificate of Calibration 6380789, American Meter Mass Flow Meter Number 10899,
        dated July 18, 2012
Unit 1 ODCM, Revision 34
Unit 1 Radioactive Effluent Release Report, January to December 2012, dated May 1, 2013
Unit 2 ODCM, Revision 35
Unit 2 UFSAR Chapter 2.3, Meteorology, Revision 19, October 2010
Section 4OA1: Performance Indicator Verification
Procedures
N2-CSP-GEN-D100, Reactor Water/Auxiliary Water Chemistry Surveillance, Revision 00601
N22-CSP-W@101, Weekly conductivity Monitor Channel Check, Revision 1
S-CAD-CHE-101, Chemistry Sample Conduct, Revision 01100
Miscellaneous
Nuclear Energy Institute 99-02, Regulatory Assessment Performance Indicator Guideline,
        Revision 6
Section 4OA2: Problem Identification and Resolution
Procedures
CENG-AM-1.01-1005, Engineering Role and Responsibilities/Expectations, Revision 00303
CNG-CA-1.01-1004, Root Cause Analysis, Revision 00802
CNG-CA-2.01-1000, Self-Assessment and Benchmarking Process, Revision 00700
CNG-MN-4.01-1001, Work Order Execution and Closure Process, Revision 00401
CNG-MN-1.01-1000, Conduct of Maintenance, Revision 00200
N2-EMP-GEN-673, 24/48 VDC and 125 VDC Batteries - Cell and Connector Replacement,
        Revision 00400
NPAP-INV-220, Storage and Handling of Material, Revision 01001
Nine Mile Point Station Policy Number 22, Work Document Quality, Revision 0
                                                                                  Attachment


Section 4OA1:  Performance Indicator Verification
                                              A-17
  Procedures
Procedure Review Briefing Sheet CNG-HU-1.01-1001 HU Tools and Verification Process
N2-CSP-GEN-D100, Reactor Water/Auxiliary Water Chemistry Surveillance, Revision 00601 N22-CSP-W@101, Weekly conductivity Monitor Channel Check, Revision 1 S-CAD-CHE-101, Chemistry Sample Conduct, Revision 01100
Understanding Human Behavior and Error, Human Reliability Associates, David Embrey
Miscellaneous
Condition Reports
Nuclear Energy Institute 99-02, Regulatory Asse
CR-1997-001696                     CR-2012-000060                    CR-2012-009469
ssment Performance Indicator Guideline,  Revision 6
CR-2001-005920                      CR-2012-001137                    CR-2012-010774
Section 4OA2:  Problem Identification and Resolution
CR-2005-003461                      CR-2012-001138                    CR-2012-010907
  Procedures
CR-2007-007514                      CR-2012-001139                    CR-2013-001159
CENG-AM-1.01-1005, Engineering Role and Re
CR-2010-001220                      CR-2012-001315                    CR-2013-002102
sponsibilities/Expectations, Revision 00303 CNG-CA-1.01-1004, Root Cause Analysis, Revision 00802 CNG-CA-2.01-1000, Self-Assessment and Benchmarking Process, Revision 00700 CNG-MN-4.01-1001, Work Order Execution and Closure Process, Revision 00401
CR-2010-001987                      CR-2012-001316                    CR-2013-002360
CNG-MN-1.01-1000, Conduct of Maintenance, Revision 00200
CR-2010-003899                      CR-2012-002716                    CR-2013-002443
N2-EMP-GEN-673, 24/48 VDC and 125 VDC Batteries - Cell and Connector Replacement, Revision 00400 NPAP-INV-220, Storage and Handling of Material, Revision 01001 Nine Mile Point Station Policy Number 22, Work Document Quality, Revision 0 
CR-2010-007337                      CR-2012-003724                    CR-2013-003207
Attachment
CR-2011-005737                      CR-2012-004600                    CR-2013-003357
A-17Procedure Review Briefing Sheet CNG-HU-1.01-1001 HU Tools and Verification Process Understanding Human Behavior and Error, Human Reliability Associates, David Embrey  
CR-2011-007171                      CR-2012-005362                    CR-2013-005074
Condition Reports
CR-2011-007269                      CR-2012-005365                    CR-2013-005117
CR-1997-001696  
CR-2011-007655                      CR-2012-006030                    CR-2013-005228
CR-2001-005920
CR-2011-009896                      CR-2012-006242                    CR-2013-005235
CR-2005-003461
CR-2011-010906                      CR-2012-006823                    CR-2013-005245
CR-2007-007514 CR-2010-001220 CR-2010-001987
CR-2011-010953                      CR-2012-007085
CR-2010-003899
CR-2011-011006                      CR-2012-007765
CR-2010-007337
Drawings
CR-2011-005737
3.N2.1-E21.1, One Line Diagram 125 VDC Control Bus, Revision 14
CR-2011-007171 CR-2011-007269 CR-2011-007655
EE-1CA, One Line Diagram Emergency and Vital Bus Power Distribution Unit 2, Revision 14
CR-2011-009896
EE-1CM, 125 VDC One Line Diagram Emergency Switchgear 2BYS*SWG002A, Revision 19
CR-2011-010906
EE-1CN, 125 VDC One Line Diagram Emergency Switchgear 2BYS*SWG002B, Revision 17
CR-2011-010953 CR-2011-011006 CR-2012-000060 CR-2012-001137
EE-MO1F, Plant Master One Line Diagram Emergency and Normal 125V and 24/48VDC Unit 2,
CR-2012-001138
      Revision 8
CR-2012-001139 CR-2012-001315 CR-2012-001316
CR-2012-002716
CR-2012-003724
CR-2012-004600
CR-2012-005362 CR-2012-005365 CR-2012-006030
CR-2012-006242
CR-2012-006823
CR-2012-007085 CR-2012-007765 CR-2012-009469 CR-2012-010774
CR-2012-010907
CR-2013-001159 CR-2013-002102 CR-2013-002360
CR-2013-002443
CR-2013-003207
CR-2013-003357
CR-2013-005074 CR-2013-005117 CR-2013-005228
CR-2013-005235
CR-2013-005245
Drawings 3.N2.1-E21.1, One Line Diagram 125 VDC Control Bus, Revision 14  
EE-1CA, One Line Diagram Emergency and Vital Bus Power Distribution Unit 2, Revision 14  
EE-1CM, 125 VDC One Line Diagram Emergen
cy Switchgear 2BYS*SWG002A, Revision 19 EE-1CN, 125 VDC One Line Diagram Emergen
cy Switchgear 2BYS*SWG002B, Revision 17 EE-MO1F, Plant Master One Line Diagram Emergency and Normal 125V and 24/48VDC Unit 2,  
Revision 8  
 
Work Orders
Work Orders
WO C92017475 WO C92036878  
WO C92017475
WO C92036878
Miscellaneous
CR Search for RCS*MOV18, Excessive Unidentified Leakage, and TS Required Shutdown for
      January 1, 2000, until April 25, 2013
Design Engineering Request NM-2001-5894
Equipment Reliability Return to Excellence Plan
Equivalency Evaluation Number 00230 for RCS*MOV 10A&B and RCS*MOV 18A&B, dated
      April 4, 2002
GE SIL No. 620, BWR 5 and 6 Reactor Recirculation System Pump Discharge Gate Valve
N2-ESP-BYS-Q767, Quarterly Battery Surveillance Test, completed on August 16 and 31, 2012;
      February 11, March 7, and May 28, 2013
N2-ESP-BYS-R685, Divisions I, II, and III Battery Modified Profile Test, completed on April 4
      and 10, 2010; April 16, July 25, and November 28, 2012
Root Cause Analysis, Cross-Cutting Theme Exists in the Aspect of Human Performance,
      Resources, Documentation H.2(c) dated January 18, 2013
Root Cause Analysis, Unit 1 SCRAM due to Turbine Trip on May 2, 2011, dated
      September 16, 2011
                                                                                      Attachment


Miscellaneous
                                                A-18
CR Search for RCS*MOV18, Excessive Unidentified Leakage, and TS Required Shutdown for January 1, 2000, until April 25, 2013 Design Engineering Request NM-2001-5894
Timeline of RCS*MOV 18A Problems
Equipment Reliability Return to Excellence Plan
Unit 1 DEP System Health Report, 1st and 2nd Quarters 2013
Equivalency Evaluation Number 00230 for
Unit 2 DEP System Health Report, 1st and 2nd Quarters 2013
RCS*MOV 10A&B and RCS*MOV 18A&B, dated  April 4, 2002 GE SIL No. 620, BWR 5 and 6 Reactor Recirculation System Pump Discharge Gate Valve 
Valve Packing Data Sheet for RCS*MOV 10A and B
N2-ESP-BYS-Q767, Quarterly Battery Surveillance Test, completed on August 16 and 31, 2012;  February 11, March 7, and May 28, 2013
Valve Packing Data Sheet for RCS*MOV 18A and B
N2-ESP-BYS-R685, Divisions I, II, and III Battery Modified Profile Test, completed on April 4  and 10, 2010; April 16, July 25, and November 28, 2012 Root Cause Analysis, Cross-Cutting Theme Exists in the Aspect of Human Performance,  Resources, Documentation H.2(c) dated January 18, 2013 Root Cause Analysis, Unit 1 SCRAM due to Turbine Trip on May 2, 2011, dated  September 16, 2011 
Vendor Manuals
Attachment
35.40, Specifications Nuclear Class 1E Flooded Batteries GNB, dated August 2002
A-18Timeline of RCS*MOV 18A Problems Unit 1 DEP System Health Report, 1
RS-1476, Stationary Battery and Vented Cell Installation and Operating Instructions C&D
st and 2 nd Quarters 2013 Unit 2 DEP System Health Report, 1
        Technologies, dated 2009
st and 2 nd Quarters 2013 Valve Packing Data Sheet for RCS*MOV 10A and B  
Calculation
Valve Packing Data Sheet for RCS*MOV 18A and B  
EC-145, Verification of Adequacy of Division III Battery 2BYS*BAT2C, Revision 2
Vendor Manuals
Section 4OA3: Follow-up of Events and Notices of Enforcement Discretion
35.40, Specifications Nuclear Class 1E Flooded Batteries GNB, dated August 2002  
Procedures
RS-1476, Stationary Battery and Vented Cell Installation and Operating Instructions C&D  
N1-OP-47A, 125 VDC Power System, Revision 02500
Technologies, dated 2009  
N1-SOP-47A.1, Loss of DC, Revision 00101
Calculation
N1-SOP-6.1, Loss of SFP/RX Cavity Level/Decay Heat Removal, Revision 00501
EC-145, Verification of Adequacy of Division III Battery 2BYS*BAT2C, Revision 2  
N1-ST-R2, LOCA and EDG Simulated Auto Initiation Test, Revision 03201
N2-EMP-GEN-609, General Small Motor Maintenance, Revision 06
NIP-OUT-01, Shutdown Safety, Revision 03700
Condition Reports
CR-2013-001633
CR-2013-002916
CR-2013-002926
CR-2013-002958
CR-2013-002998
Miscellaneous
ACE for CR-2013-001633
CENG Safety Stand Down for April 16, 2013, Loss of Battery Bus 12 Event
Control Room Operator Logs for Tuesday, April 16, 2013
E191, NMPNS Specification for Safety-Related Motor Repairs, Revision 0
Outage Control Center Logs for Tuesday, April 16, 2013
PM Template for Small and Intermediate HP Motors
Unit 1 Station Alarm Log for Tuesday, April 16, 2013
Work Control Center Turnover Sheet for April 16, 2013, Days to Night
                                                                                      Attachment


Section 4OA3:  Follow-up of Events and Notices of Enforcement Discretion
                                A-19
    
                        LIST OF ACRONYMS
Procedures
10 CFR Title 10 of the Code of Federal Regulations
N1-OP-47A, 125 VDC Power System, Revision 02500
AC    alternating current
N1-SOP-47A.1, Loss of DC, Revision 00101
ADAMS  Agencywide Documents Access and Management System
N1-SOP-6.1, Loss of SFP/RX Cavity Level/Decay Heat Removal, Revision 00501
ALARA  as low as reasonably achievable
N1-ST-R2, LOCA and EDG Simulated Auto Initiation Test, Revision 03201 N2-EMP-GEN-609, General Small Motor Maintenance, Revision 06 NIP-OUT-01, Shutdown Safety, Revision 03700
ASME  American Society of Mechanical Engineers
Condition Reports
BWR   boiling-water reactor
CR-2013-001633 CR-2013-002916 CR-2013-002926
CAP    corrective action program
CR-2013-002958 CR-2013-002998
CENG  Constellation Energy Nuclear Group, LLC
Miscellaneous
DC     direct current
ACE for CR-2013-001633 CENG Safety Stand Down for April 16, 2013, Loss of Battery Bus 12 Event Control Room Operator Logs for Tuesday, April 16, 2013 E191, NMPNS Specification for Safety-Related Motor Repairs, Revision 0 Outage Control Center Logs for Tuesday, April 16, 2013 PM Template for Small and Intermediate HP Motors Unit 1 Station Alarm Log for Tuesday, April 16, 2013
ECCS  emergency core cooling system
Work Control Center Turnover Sheet for April 16, 2013, Days to Night
ECP    engineering change package
EDG    emergency diesel generator
ERV    electro-matic relief valve
FA    fire area
FAC    flow accelerated corrosion
FCV    flow control valve
HPCS  high-pressure core spray
I&C    instrumentation and control
IEEE  Institute of Electrical and Electronics Engineers
IMC    Inspection Manual Chapter
ISI    inservice inspection
kV    kilovolt
LER    licensee event report
LOCA   loss of coolant accident
LOOP  loss of offsite power
NDE    nondestructive examination
NCV    non-cited violation
NMPNS  Nine Mile Point Nuclear Station, LLC
NRC    Nuclear Regulatory Commission
ODCM  offsite dose calculation manual
psig  pounds per square inch gauge
RB    reactor building
RCIC  reactor core isolation cooling
RCS    reactor coolant system
REMP  radiological environmental monitoring program
RG    regulatory guide
RHR    residual heat removal
RPT    radiation protection technician
RPV    reactor pressure vessel
RWCU  reactor water cleanup
RWP    radiation work permit
SDC    shutdown cooling
SDP    significance determination process
SFP    spent fuel pool
SSC    structure, system, and component
                                                        Enclosure


 
                              A-20
A-19 Enclosure
ST    surveillance testing
LIST OF ACRONYMS
TLD  thermo luminescent dosimeter
 
TS   technical specification
10 CFR  Title 10 of the
UFSAR Updated Final Safety Analysis Report
Code of Federal Regulations
UT   ultrasonic testing
  AC  alternating current
ADAMS  Agencywide Documents Access and Management System ALARA  as low as reasonably achievable ASME  American Society of Mechanical Engineers
BWR  boiling-water reactor
CAP  corrective action program
CENG  Constellation Energy Nuclear Group, LLC DC  direct current ECCS  emergency core cooling system
ECP  engineering change package
EDG  emergency diesel generator
ERV  electro-matic relief valve
FA  fire area FAC  flow accelerated corrosion FCV  flow control valve
HPCS  high-pressure core spray
I&C  instrumentation and control
IEEE  Institute of Electrical and Electronics Engineers IMC  Inspection Manual Chapter ISI  inservice inspection
kV  kilovolt
LER  licensee event report
LOCA  loss of coolant accident LOOP  loss of offsite power NDE  nondestructive examination
NCV  non-cited violation
NMPNS  Nine Mile Point Nuclear Station, LLC
NRC  Nuclear Regulatory Commission
ODCM  offsite dose calculation manual psig  pounds per square inch gauge RB  reactor building
RCIC  reactor core isolation cooling
RCS  reactor coolant system
REMP  radiological environmental monitoring program RG  regulatory guide RHR  residual heat removal
RPT  radiation protection technician
RPV  reactor pressure vessel
RWCU  reactor water cleanup
RWP  radiation work permit SDC  shutdown cooling SDP  significance determination process
SFP  spent fuel pool
SSC  structure, system, and component 
Attachment
A-20ST  surveillance testing TLD  thermo luminescent dosimeter TS   technical specification UFSAR Updated Final Safety Analysis Report  
UT   ultrasonic testing  
VDC  volts direct current
VDC  volts direct current
                                          Attachment
}}
}}

Latest revision as of 14:48, 4 November 2019

IR 05000220-13-003, 05000410-13-003; on 04/01/2013 - 06/30/2013; Nine Mile Point Nuclear Station (NMPNS) Units 1 and 2; Surveillance Testing, Problem Identification and Resolution, Follow-Up of Events and Notices of Enforcement Discretion
ML13225A471
Person / Time
Site: Nine Mile Point  Constellation icon.png
Issue date: 08/13/2013
From: Daniel Schroeder
Reactor Projects Branch 1
To: Costanzo C
Constellation Energy Nuclear Group
Schroeder D
References
IR-13-003
Download: ML13225A471 (73)


See also: IR 05000220/2013003

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION I

2100 RENAISSANCE BOULEVARD, SUITE 100

KING OF PRUSSIA, PENNSYLVANIA 19406-2713

August 13, 2013

Mr. Christopher Costanzo, Vice President

Nine Mile Point Nuclear Station

Constellation Energy Nuclear Group, LLC

P.O. Box 63

Lycoming, NY 13093

SUBJECT: NINE MILE POINT NUCLEAR STATION - NRC INTEGRATED INSPECTION

REPORT 05000220/2013003 AND 05000410/2013003

Dear Mr. Costanzo:

On June 30, 2013, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at

your Nine Mile Point Nuclear Station (NMPNS) Units 1 and 2. The enclosed inspection report

documents the inspection results, which were discussed on July 25, 2013, with you and other

members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

This report documents one self-revealing apparent violation concerning the improper restoration

of a direct current electrical bus which resulted in a loss of all shutdown cooling. The safety

significance of the violation is still under review pending the outcome of a Phase III risk analysis

by NRC Senior Reactor Analysts. However, the violation does not represent an immediate

safety concern because Constellation has conducted a prompt human performance event

review, entered the issue into their corrective action program (CAP), and conducted a root

cause analysis. Additionally, corrective actions including a review of all emergency, off-normal,

and normal system operating procedures are in progress. This violation with the supporting

circumstances and details is documented in this inspection report.

This report documents two NRC-identified findings and two self-revealing findings of very low

safety significance (Green). These findings were determined to involve violations of NRC

requirements. However, because of the very low safety significance, and because they are

entered into your CAP, the NRC is treating these findings as non-cited violations (NCVs)

consistent with Section 2.3.2 of the NRC Enforcement Policy. If you contest any NCVs in this

report, you should provide a response within 30 days of the date of this inspection report with

the basis of your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control

Desk, Washington D.C. 20555-0001; with copies to the Regional Administrator, Region I; the

Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, D.C.

20555-0001; and the NRC Resident Inspector at NMPNS. In addition, if you disagree with the

C. Costanzo 2

cross-cutting aspect assigned to any finding in this report, you should provide a response within

30 days of the date of this inspection report, with the basis for your disagreement, to the

Regional Administrator, Region I, and the NRC Resident Inspector at NMPNS.

In accordance with Title 10 of the Code of Federal Regulations 2.390 of the NRCs Rules of

Practice, a copy of this letter, its enclosure, and your response (if any) will be available

electronically for public inspection in the NRC Public Document Room or from the Publicly

Available Records component of the NRCs Agencywide Documents Access Management

System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-

rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Daniel L. Schroeder, Chief

Reactor Projects Branch 1

Division of Reactor Projects

Docket Nos: 50-220 and 50-410

License Nos: DPR-63 and NPF-69

Enclosure: Inspection Report 05000220/2013003 and 05000410/2013003

w/Attachment: Supplementary Information

cc w/encl: Distribution via ListServ

ML13225A471

Non-Sensitive Publicly Available

SUNSI Review

Sensitive Non-Publicly Available

OFFICE klm RI/DRP RI/DRP RI/DRP

NAME KKolaczyk/DLS for ARosebrook/DLS for DSchroeder/DLS

DATE 08/13/13 08/13/13 08/13/13

1

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

Docket Nos: 50-220 and 50-410

License Nos: DPR-63 and NPF-69

Report No: 05000220/2013003 and 05000410/2013003

Licensee: Constellation Energy Nuclear Group, LLC (CENG)

Facility: Nine Mile Point Nuclear Station, Units 1 and 2

Location: Oswego, NY

Dates: April 1, 2013 through June 30, 2013

Inspectors: K. Kolaczyk, Senior Resident Inspector

E. Miller, Resident Inspector

B. Dionne, Health Physicist

B. Haagensen, Resident Inspector

P. Kaufman, Senior Reactor Inspector

J. Krafty, Resident Inspector

J. Laughlin, Emergency Preparedness Inspector

J. Lilliendahl, Reactor Inspector

A. Rosebrook, Senior Project Engineer

B. Scrabeck, Project Engineer

Approved by: Daniel L. Schroeder, Chief

Reactor Projects Branch 1

Division of Reactor Projects

Enclosure

2

TABLE OF CONTENTS

SUMMARY.................................................................................................................................... 3

1. REACTOR SAFETY.............................................................................................................. 7

1R01 Adverse Weather Protection ................................................................................... 7

1R04 Equipment Alignment .............................................................................................. 8

1R05 Fire Protection ......................................................................................................... 9

1R07 Heat Sink Performance ........................................................................................... 9

1R08 Inservice Inspection Activities ............................................................................... 10

1R11 Licensed Operator Requalification Program & Licensed Operator Performance .. 12

1R12 Maintenance Effectiveness ................................................................................... 13

1R13 Maintenance Risk Assessments and Emergent Work Control .............................. 13

1R15 Operability Determinations and Functionality Assessments.................................. 14

1R18 Plant Modifications ................................................................................................ 15

1R19 Post-Maintenance Testing ..................................................................................... 15

1R20 Refueling and Other Outage Activities .................................................................. 16

1R22 Surveillance Testing .............................................................................................. 17

1EP4 Emergency Action Level and Emergency Plan Changes ...................................... 20

1EP6 Drill Evaluation ...................................................................................................... 20

2. RADIATION SAFETY.......................................................................................................... 21

2RS1 Radiological Hazard Assessment and Exposure Controls .................................... 21

2RS2 Occupational ALARA Planning and Controls ........................................................ 24

2RS3 In-Plant Airborne Radioactivity Control and Mitigation .......................................... 26

2RS4 Occupational Dose Assessment ........................................................................... 27

2RS7 Radiological Environmental Monitoring Program .................................................. 30

4. OTHER ACTIVITIES ........................................................................................................... 33

4OA1 Performance Indicator Verification ........................................................................ 33

4OA2 Problem Identification and Resolution ................................................................... 33

4OA3 Follow-Up of Events and Notices of Enforcement Discretion ................................ 42

4OA6 Meetings, Including Exit ........................................................................................ 50

ATTACHMENT: SUPPLEMENTARY INFORMATION .............................................................. 50

SUPPLEMENTARY INFORMATION ........................................................................................ A-1

KEY POINTS OF CONTACT .................................................................................................... A-1

LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED ..................................... A-2

LIST OF DOCUMENTS REVIEWED ........................................................................................ A-3

LIST OF ACRONYMS............................................................................................................. A-19

Enclosure

3

SUMMARY

IR 05000220/2013003, 05000410/2013003; 04/01/2013 - 06/30/2013; Nine Mile Point Nuclear

Station (NMPNS) Units 1 and 2; Surveillance Testing, Problem Identification and Resolution,

Follow-Up of Events and Notices of Enforcement Discretion.

This report covered a 3-month period of inspection by resident inspectors and announced

inspections performed by regional inspectors. One apparent violation was identified. The

safety significance of this violation is still under review pending the outcome of a Phase III risk

analysis by NRC Senior Reactor Analysts. Additionally, two NRC-identified findings and two

self-revealing findings of very low safety significance (Green) were identified, all of which were

non-cited violations (NCVs). The significance of most findings is indicated by their color (i.e.,

greater than Green, or Green, White, Yellow, Red) and determined using Inspection Manual

Chapter (IMC) 0609, Significance Determination Process (SDP), dated June 2, 2011. Cross-

cutting aspects are determined using IMC 0310, Components Within the Cross-Cutting Areas,

dated October 28, 2011. All violations of NRC requirements are dispositioned in accordance

with the NRCs Enforcement Policy, dated January 28, 2013. The NRCs program for

overseeing the safe operation of commercial nuclear power reactors is described in NUREG-

1649, Reactor Oversight Process, Revision 4.

Cornerstone: Initiating Events

TBD. A self-revealing apparent violation of Technical Specification (TS) 6.4.1, Procedures,

was identified at Unit 1 because CENG failed to properly recover from a loss of a vital direct

current (DC) bus in accordance with station off-normal procedures resulting in an unplanned

loss of all shutdown cooling (SDC) when time to boil was less than 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />. Specifically,

during the restoration from the loss of battery bus 12, operators failed to identify a SDC trip

signal before attempting restoration of the DC bus, which ultimately lead to a SDC pump trip

(i.e. loss of decay heat removal from the reactor). Corrective actions included conducting a

prompt human performance event review, entering the issue into their corrective action

program (CAP), and conducting a root cause analysis. Planned corrective actions include a

review of all emergency, off-normal, and normal system operating procedures.

The inspectors determined that CENGs failure to properly restore battery bus 12 in

accordance with N1-SOP-47A.1, Loss of DC, Revision 00101, and N1-OP-47A, 125 VDC

Power System, Revision 02500, was a performance deficiency that was reasonably within

CENGs ability to foresee and correct and should have been prevented. The performance

deficiency was determined to be more than minor because the inspectors determined it

affected the configuration control aspect of the Initiating Events cornerstone and adversely

affected the associated cornerstone objective to limit the likelihood of events that upset plant

stability and challenge critical safety functions during shutdown as well as power operations.

The significance of the finding is designated as To Be Determined (TBD) until a Phase 3

analysis can be completed by the NRCs Senior Reactor Analysts. The inspectors

determined this finding has a cross-cutting aspect in the area of Human Performance,

Resources, because CENG did not ensure that personnel, equipment, procedures, and

other resources were available and adequate to assure nuclear safety - complete, accurate

Enclosure

4

and up-to-date design documentation, procedures, work packages, and correct labeling of

components. Specifically, CENG procedures N1-SOP-47A.1 and N1-OP-47A did not

contain adequate guidance to ensure recovery from a loss of a DC bus would not result in

an unexpected plant transient H.2(c). (Section 4OA3)

Cornerstone: Mitigating Systems

Green. A self-revealing NCV of TS 5.4.1, Procedures, was identified at Unit 2 when a

CENG instrumentation and control (I&C) technician did not properly implement procedure

N2-ISP-LDS-Q010, Reactor Building General Area Temperature Instrument Channel

Functional Test, Revision 00102. As a result, a residual heat removal (RHR)/reactor core

isolation cooling (RCIC) isolation bypass switch was inadvertently left in the NORMAL

position during surveillance testing resulting in an unplanned RCIC isolation. CENG entered

this issue into their CAP as CR-2013-002461. Other corrective actions included performing

a human performance stand down that reinforced use of human performance tools and the

need to identify and mark critical steps during pre-job briefs, retraining the I&C technicians

involved in the event on proper use of human performance error prevention techniques, and

improving bypass switch verification steps for procedure N2-ISP-LDS-Q010 and other

similar lead detection system surveillances procedures.

This finding is more than minor because it is associated with the human performance

attribute of the Mitigating Systems cornerstone and affected the cornerstone objective to

ensure the availability, reliability, and capability of systems that respond to initiating events

to prevent undesirable consequences (i.e., core damage). Specifically, the inadvertent

isolation rendered the RCIC system inoperable and unable to perform its function for

approximately 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. Additionally, this finding is similar to example 4.b of IMC 0612,

Appendix E, Examples of Minor issues, and is more than minor due to the procedural error

leading to a plant transient, i.e. an unplanned RCIC isolation. This finding was evaluated in

accordance with IMC 0609.04, Initial Characterization of Findings, and Exhibit 2 of IMC

0609, Appendix A, The Significance Determination Process for Findings At-Power, issued

June 19, 2012. Unit 2 is a boiling-water reactor (BWR)-5, and as a result, RCIC is treated

as having a separate high-pressure injection safety function. A detailed analysis was

conducted using SAPHIRE version 8.0.8.0 and Unit 2 SPAR model 8.17. Using an

exposure period of 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and conservatively assuming no recovery of the failed

equipment, this finding had a change in core damage frequency of low E-8. The dominant

accident sequence was a grid-related loss of offsite power with a failure of Division III power

and the failure to recover offsite power and the emergency diesel generators (EDGs) in 30

minutes. Since the change in core damage frequency was less than 1E-7, contributions

from large early release and external event did not need to be considered. Therefore, this

finding was of very low safety significance (Green). This finding has a cross-cutting aspect

in the area of Human Performance, Work Practices, because the I&C technicians did not

effectively employ self-checking and place-keeping when implementing the test procedure

which directly contributed to the resulting procedural error H.4(a). (Section 1R22)

Green. The inspectors identified an NCV at Unit 2 of Title 10 of the Code of Federal

Regulations (10 CFR) Part 50, Appendix B, Criterion V, Instructions, Procedures, and

Drawings, because CENG did not assure that the replacement of cells in battery 2C were

prescribed and performed by appropriate procedures which resulted in degraded accuracy

Enclosure

5

of test results and potential degradation of safety-related battery cells. In response to this

issue, CENG generated CR-2013-005235 and initiated actions to evaluate replacing the

new cells.

This finding is more than minor because it was associated with the equipment performance

attribute of the Mitigating Systems cornerstone and affected the cornerstone objective to

ensure the availability, reliability, and capability of systems that respond to initiating events

to prevent undesirable consequences. In accordance with IMC 0609.04, Initial

Characterization of Findings, and Exhibit 2 of IMC 0609, Appendix A, The Significance

Determination Process for Findings At-Power, issued June 19, 2012, the inspectors

determined this finding is of very low safety significance (Green) because the performance

deficiency was not a design or qualification deficiency, did not involve an actual loss of

safety function, did not represent actual loss of a safety function of a single train for greater

than its TS allowed outage time, and did not screen as potentially risk-significant due to a

seismic, flooding, or severe weather initiating event. This finding has a cross-cutting aspect

in the area of Human Performance, Decision-Making component, because CENG did not

use conservative assumptions in decision making. Specifically, CENG did not monitor the

cells in storage, question the adequacy of the discharged cells, charge the cells prior to

installation, or fully evaluate the implications of the test and recharge results H.1(b).

(Section 4OA2)

Green. The inspectors identified an NCV at Unit 2 of 10 CFR Part 50, Appendix B,

Criterion III, Design Control, because CENG did not verify the adequacy of the design with

respect to battery 2C. Specifically, by failing to size the battery to the most limiting time

period, the sizing calculation significantly overstated the available design margin. CENGs

corrective actions included generating condition report CR-2013-005117 and evaluating the

condition for operability.

This finding is more than minor because it was associated with the design control attribute of

the Mitigating Systems cornerstone and affected the cornerstone objective to ensure the

availability, reliability, and capability of systems that respond to initiating events to prevent

undesirable consequences. In accordance with IMC 0609.04, Initial Characterization of

Findings, and Exhibit 2 of IMC 0609, Appendix A, The Significance Determination Process

for Findings At-Power, issued June 19, 2012, the inspectors determined this finding is of

very low safety significance (Green) because the performance deficiency was not a design

or qualification deficiency, did not involve an actual loss of safety function, did not represent

actual loss of a safety function of a single train for greater than its TS allowed outage time,

and did not screen as potentially risk-significant due to a seismic, flooding, or severe

weather initiating event. The inspectors did not assign a cross-cutting aspect because the

finding was not indicative of current performance. (Section 4OA2)

Cornerstone: Barrier Integrity

Green. A self-revealing NCV of TS 3.3.3, Leakage Rate, was identified for CENGs failure

from December 3 to December 13, 2012, to maintain containment leakage less than

1.5 percent by weight of the containment air per day and less than 0.6 percent by weight of

the containment air per day for all penetrations and all primary containment isolation valves

subject to 10 CFR Part 50, Appendix J, Types B and C tests, when pressurized to

Enclosure

6

35 pound per square inch gauge when reactor coolant system (RCS) temperature is above

215°F and primary containment integrity is required. CENG entered this issue into their

CAP as CR-2012-011247. Corrective actions included cleaning iron oxide from the primary

containment vent and purge valve and replacing the resilient seals.

This finding is more than minor because it is associated with the structure, system,

component (SSC), and barrier performance attribute of the Barrier Integrity cornerstone and

affected the cornerstone objective to provide reasonable assurance that physical design

barriers (fuel cladding, reactor coolant system, and containment) protect the public from

radionuclide releases caused by accidents or events. Specifically, containment leakage

exceeded the leakage limits outlined in the Unit 1 TS 3.3.3 from December 3 to December

13, 2012. This finding was evaluated in accordance with IMC 0609.04, Initial

Characterization of Findings, and Table 6.2, Phase 2 Risk Significance-Type B Findings at

Full Power, of IMC 0609, Appendix H, Containment Integrity Significance Determination

Process, issued May 6, 2004. The inspectors determined this finding was of very low

safety significance (Green) because the leakage was less than 100 percent of containment

volume per day for the duration of the leak. This finding has a cross-cutting aspect in the

area of Problem Identification and Resolution, CAP, because CENG failed to take

appropriate corrective action to address safety issues and adverse trends in a timely

manner commensurate with their safety significance. Specifically, following identification of

the adverse trend regarding the frequency of nitrogen addition to the drywell, CENG did not

assess in a timely manner the significance of the leakage and the impact on primary plant

containment P.1(d). (Section 4OA3)

Enclosure

7

REPORT DETAILS

Summary of Plant Status

Unit 1 began the inspection period at 100 percent power. On April 14, 2013, Unit 1 reduced

power to 32 percent to conduct emergency condenser testing and to down power for refueling

outage (N1R22). On April 15, Unit 1 was removed from the grid to commence N1R22. Unit 1

returned to service and synchronized to the grid on May 15. On June 21, Unit 1 down powered

to 83 percent to perform a rod pattern adjustment, turbine stop valve replacement, and a reactor

recirculation pump swap. Unit 1 returned to rated power on June 22 and remained at or near

full power for the remainder of the inspection period.

Unit 2 began the inspection period at 100 percent power. On May 28, Unit 2 down powered to

65 percent to investigate diverging feedwater flows between two operating feedwater pumps.

Following identification of a degraded automatic feedwater regulating valve and removal of the

B feedwater pump from service, Unit 2 returned to 100 percent on May 31, and remained at or

near full power for the remainder of the inspection period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection (71111.01 - 2 samples)

.1 Readiness for Seasonal Extreme Weather Conditions

a. Inspection Scope

The inspectors performed a review of CENGs readiness for the onset of seasonal high

temperatures. The review focused on Unit 1 fire protection and diesel fire pump,

technical support center ventilation, control room and reactor building (RB) air

conditioning systems, and Unit 2 service water and heating, ventilation, and air

conditioning systems. The inspectors reviewed the Updated Final Safety Analysis

Report (UFSAR), TSs, and the CAP to determine what temperatures or other seasonal

weather could challenge these systems and to ensure CENG personnel had adequately

prepared for these challenges. The inspectors reviewed station procedures including

CENGs seasonal weather readiness procedure and applicable operating procedures.

The inspectors performed walkdowns of the selected systems to ensure station

personnel identified issues that could challenge the operability of the systems during hot

weather conditions. Documents reviewed for each section of this inspection report are

listed in the Attachment.

b. Findings

No findings were identified.

Enclosure

8

.2 Summer Readiness of Offsite and Alternate Alternating Current (AC) Power Systems

a. Inspection Scope

The inspectors performed a review of plant features and procedures for the operation

and continued availability of the offsite and alternate AC power system to evaluate

readiness of the systems prior to seasonal high grid loading. The inspectors reviewed

changes to CENGs procedures affecting these areas and the communications protocols

between the transmission system operator and CENG implemented since the previous

sample in 2012. This review focused on changes to the established program and

material condition of the offsite and alternate AC power equipment. The inspectors

assessed whether CENG established and implemented appropriate procedures and

protocols to monitor and maintain availability and reliability of both the offsite ac power

system and the onsite alternate AC power system. The inspectors evaluated the material

condition of the associated equipment by interviewing the season readiness coordinator,

reviewing condition reports and open work orders and walking down portions of the

offsite and AC power systems including the 345 kilovolt (kV) and 115 kV switchyards.

b. Findings

No findings were identified.

1R04 Equipment Alignment

Partial System Walkdown (71111.04Q - 5 samples)

a. Inspection Scope

The inspectors performed partial walkdowns of the following systems:

Unit 1, Spent fuel pool (SFP) cooling system during the conduct of refueling

maintenance related activities on April 15, 2013

Unit 1, Core sprays 112 and 122 following the completion of surveillance activities on

April 21, 2013

Unit 1, Isolation condenser loop 12 following the completion of maintenance activities

on May 15, 2013

Unit 1, Diesel and electric fire pumps while the maintenance fire pump was operating

with a degraded discharge relief valve on May 22, 2013

Unit 1, Control room emergency ventilation system following the completion of

maintenance activities on May 30, 2013

The inspectors selected these systems based on their risk-significance relative to the

reactor safety cornerstones at the time they were inspected. The inspectors reviewed

applicable operating procedures, system diagrams, the UFSAR, TSs, work orders,

condition reports, and the impact of ongoing work activities on redundant trains of

equipment in order to identify conditions that could have impacted system performance

of their intended safety functions. The inspectors also performed field walkdowns of

accessible portions of the systems to verify system components and support equipment

were aligned correctly and were operable. The inspectors examined the material

condition of the components and observed operating parameters of equipment to verify

Enclosure

9

that there were no deficiencies. The inspectors also reviewed whether CENG staff had

properly identified equipment issues and entered them into the CAP for resolution with

the appropriate significance characterization.

b. Findings

No findings were identified.

1R05 Fire Protection

Resident Inspector Quarterly Walkdowns (71111.05Q - 6 samples)

a. Inspection Scope

The inspectors conducted tours of the areas listed below to assess the material

condition and operational status of fire protection features. The inspectors verified that

CENG controlled combustible materials and ignition sources in accordance with

administrative procedures. The inspectors verified that fire protection and suppression

equipment was available for use as specified in the area pre-fire plan, and passive fire

barriers were maintained in good material condition. The inspectors also verified that

station personnel implemented compensatory measures for out of service, degraded, or

inoperable fire protection equipment, as applicable, in accordance with procedures.

Unit 1, Drywell (FA3/R1) on April 16, 2013

Unit 1, RB elevation 340 feet (FA1/R6A and FA2/R6B) on April 19, 2013

Unit 1, RB elevation 198 feet southwest (FA2/R1B) on April 21, 2013

Unit 1, RB elevation 237 feet east (FA1/R1A) on April 21, 2013

Unit 1, RB elevation 237 feet west (FA2/R1B) on April 21, 2013

Unit 1, Power board 12 (FA-17A) on April 26, 2013

b. Findings

No findings were identified.

1R07 Heat Sink Performance (71111.07 - 2 samples)

a. Inspection Scope

The inspectors reviewed the samples listed below to determine their readiness and

availability to perform their safety functions. The inspectors reviewed the design basis

for the components and verified CENGs commitments to NRC Generic Letter 89-13.

The inspectors discussed the results of the most recent inspection with engineering staff

and reviewed pictures of the as-found and as-left conditions. The inspectors verified that

CENG initiated appropriate corrective actions for identified deficiencies.

Unit 1, Emergency diesel generator (EDG) 103 raw water heat exchanger on

May 3, 2013

Unit 2, 2HVY*UC2A service water pump bay A unit cooler on May 7, 2013

Enclosure

10

1R08 Inservice Inspection Activities (71111.08 - 1 sample)

a. Inspection Scope

From April 15 to 18, 2013, the inspectors conducted a review of CENGs implementation

of inservice inspection (ISI) program activities for monitoring degradation of the RCS

boundary and risk-significant piping system boundaries for Unit 1 during the N1R22.

The sample selection was based on the inspection procedure objectives and risk priority

of those components and systems where degradation would result in a significant

increase in risk of core damage. The inspectors observed in-process nondestructive

examinations (NDEs), reviewed documentation, and interviewed CENG personnel to

verify that the NDE activities performed were conducted in accordance with the

requirements of the American Society of Mechanical Engineers (ASME) Boiler and

Pressure Vessel Code,Section XI, 2004 Edition.

NDE Activities and Welding Activities

The inspectors performed direct observations of NDE activities in process and reviewed

records of NDEs listed below:

ASME Code Required Examinations

Remote visual examination (VT-3) of reactor vessel nozzle N16-1-N3A and manual

ultrasonic testing (UT) examination of three 12-inch diameter emergency condenser

supply piping welds.

Data records of manual UT phased array examination of five 28-inch diameter

reactor vessel nozzle-to-vessel dissimilar metal safe end-to-nozzle welds (32-WD-

042, N2A; 32-WD-082, N2B; 32-WD-122, N2C; 32-WD-164, N2D; 32-WD-208, N2E),

manual UT of four 12-inch diameter emergency condenser supply piping welds, dye

penetrant testing and UT of branch connection-decontamination port welds on the

recirculation system suction piping, and UT thickness readings of various diameter

RB closed loop cooling system piping located at elevation 225 foot in the drywell.

The inspectors reviewed certifications of the NDE technician, process, and equipment in

identifying the condition or degradation of risk-significant SSCs and evaluated the

activities for compliance with the requirements of Unit 1s risk informed ISI program,

ASME Boiler and Pressure Vessel Code,Section XI, and 10 CFR 50.55a.

Augmented or Industry Imitative Examinations

Based on industry operating experience, the inspectors reviewed NDE data records of

the recirculation system suction piping decontamination port branch connection welds to

verify that the activities were performed in accordance with applicable examination

procedures and industry guidance.

Modification/Repair/Replacement Consisting of Welding Activities

The inspectors reviewed the following welding activities to verify specifications and

control of the welding processes, weld procedures, welder qualifications, and NDE

examinations were in accordance with ASME code requirements.

Enclosure

11

The repair and replacement of reactor water cleanup (RWCU) dissimilar metal pipe weld

33-WD-046 was reviewed. The inspectors reviewed the associated flaw evaluation,

NDE data records, and repair/replacement WO package.

During manual phased array UT of a 6-inch diameter schedule 80 stainless steel pipe to

carbon steel RWCU pipe dissimilar metal weld, a 4.25-inch long circumferential flaw

indication was detected in the heat-affected zone of the stainless steel side of the weld.

The indication did not meet ASME Code,Section XI 2004, IWB-3514-2 acceptance

criteria so a flaw evaluation was required. The flaw evaluation concluded that sufficient

structural margin was demonstrated for the as-found flaw indication.

However, a review of construction radiographs by CENG indicated that there had been

two previous weld repairs directly adjacent to this indication. CENG determined that the

residual stresses of the weld were likely to be high due to the prior weld repairs and the

crack growth rate would be high enough to possibly propagate the flaw beyond the

ASME code limit of through-thickness. Based on this information, CENG replaced the

weld and adjacent pipe by installing a new spool piece.

The inspectors verified the welding activities and applicable NDE techniques were

performed in accordance with ASME Code requirements.

Re-examination of an Indication Previously Accepted for Service After Analysis

There were no samples available for review during this inspection that involved

examinations with recordable indications that have been accepted for continued service

from the previous Unit 1 outage through the current outage.

Drywell Visual Examination

The inspectors examined the condition of Unit 1 drywell liner surface at various elevation

levels inside the drywell. During the inspection, surface corrosion was noted on the

drywell liner and on several systems including the RB closed-cooling water system.

CENG was monitoring the condition of the liner and RB closed-cooling water system to

ensure the corrosion was not impacting system or component operability.

Identification and Resolution of Problems

The inspectors reviewed a sample of condition reports which involved ISI-related

activities to confirm that non-conformances were being properly identified, reported, and

resolved.

b. Findings

No findings were identified.

Enclosure

12

1R11 Licensed Operator Requalification Program and Licensed Operator Performance

(71111.11Q - 4 samples)

.1 Quarterly Review of Licensed Operator Requalification Testing and Training (2 samples)

a. Inspection Scope

The inspectors observed:

Unit 1, Licensed operator simulator training which included a loss of condenser

vacuum, a stuck open electro-matic relief valve (ERV), and an anticipated transient

without scram on April 2, 2013

Unit 2, Licensed operator performance during a simulator training scenario that

included high temperatures on the main transformer, degraded service water, and a

loss of the offsite electrical grid on May 23, 2013

The inspectors evaluated operator performance during the simulated event and verified

completion of risk-significant operator actions, including the use of abnormal and

emergency operating procedures. The inspectors assessed the clarity and effectiveness

of communications, implementation of actions in response to alarms and degrading plant

conditions, and the oversight and direction provided by the control room supervisor. The

inspectors verified the accuracy and timeliness of the emergency classifications made by

the shift manager and the TS action statements entered by the shift technical advisor.

Additionally, the inspectors assessed the ability of the crew and training staff to identify

and document crew performance problems.

b. Findings

No findings were identified.

.2 Quarterly Review of Licensed Operator Performance in the Main Control Room

(2 samples)

a. Inspection Scope

The inspectors observed:

Unit 2, Control room operations during a period of increased site activity due to a

failure of an on-site power loop that supplied electrical power to several non-

essential buildings within the protected area as well as several plant information

technology systems on April 9, 2013

Unit 1, Control room operations during a plant shutdown to commence planned

refueling outage N1R22 on April 14, 2013

The inspectors reviewed CNG-OP-1.01-1000, Conduct of Operations, Revision 00900,

and verified that procedure use, crew communications, and coordination of plant

activities among work groups similarly met established expectations and standards.

Additionally, the inspectors observed test performance to verify that procedure use, crew

communications, and coordination of activities between work groups similarly met

established expectations and standards.

Enclosure

13

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness (71111.12Q - 4 samples)

a. Inspection Scope

The inspectors reviewed the samples listed below to assess the effectiveness of

maintenance activities on SSC performance and reliability. The inspectors reviewed

system health reports, CAP documents, maintenance work orders, and maintenance

rule basis documents to ensure that CENG was identifying and properly evaluating

performance problems within the scope of the maintenance rule. For each sample

selected, the inspectors verified that the SSC was properly scoped into the maintenance

rule in accordance with 10 CFR 50.65 and verified that the (a)(2) performance criteria

established by CENG staff was reasonable. As applicable, for SSCs classified as (a)(1),

the inspectors assessed the adequacy of goals and corrective actions to return these

SSCs to (a)(2). Additionally, the inspectors ensured that CENG staff was identifying and

addressing common cause failures that occurred within and across maintenance rule

system boundaries.

Unit 1, Neutron monitoring on May 14, 2013

Unit 2, High-pressure core spray (HPCS) on May 14, 2013

Unit 1, Service water on May 16, 2013

Unit 1, Containment spray on May 17, 2013

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13 - 8 samples)

a. Inspection Scope

The inspectors reviewed station evaluation and management of plant risk for the

maintenance and emergent work activities listed below to verify that CENG performed

the appropriate risk assessments prior to removing equipment from service. The

inspectors selected these activities based on potential risk significance relative to the

reactor safety cornerstones. As applicable for each activity, the inspectors verified that

CENG personnel performed risk assessments as required by 10 CFR 50.65(a)(4) and

that the assessments were accurate and complete. When CENG performed emergent

work, the inspectors verified that operations personnel promptly assessed and managed

plant risk. The inspectors reviewed the scope of maintenance work and discussed the

results of the assessment with the stations probabilistic risk analyst to verify plant

conditions were consistent with the risk assessment. The inspectors also reviewed the

TS requirements and inspected portions of redundant safety systems, when applicable,

to verify risk analysis assumptions were valid and applicable requirements were met.

Enclosure

14

Unit 2, Unplanned elevated risk condition that resulted from an inadvertent isolation

of the RCIC system on April 2, 2013

Unit 2, Loss of maintenance supply power to 2VBB*UPS3B on April 5, 2013

Unit 1, Power boards 102 and 16 following electrical realignment on May 1, 2013

Unit 1, Planned maintenance on pressure safety valve 201.970, emergency

condenser vent isolation IV-05-03, and emergency condenser 112 HX HTX-60-44 on

May 2, 2013

Unit 2, Planned maintenance on the Division I control room air conditioning system

on May 13, 2013

Unit 1, Unplanned maintenance on the turbine bypass valve control system on

May 14, 2013

Unit 1, Planned maintenance on the 102 EDG raw water pump on May 23, 2013

Unit 2, Unplanned maintenance on the 2SWP*P1B service water pump on June 11,

2013

b. Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessments (71111.15 - 9 samples)

a. Inspection Scope

The inspectors reviewed operability determinations for the following degraded or non-

conforming conditions:

Unit 1, Acceptance criteria associated with N1-ST-C5, secondary containment, and

RB emergency ventilation system operability testing on April 13, 2013

Unit 1, Emergency service water 11 pump (72-04) trip during surveillance testing on

April 17, 2013

Unit 1, Damaged containment spray nozzle deflectors on May 3, 2013

Unit 1, Source range monitors due to under-vessel work on May 3, 2013

Unit 1, Steam leakage from vent valve 05-11 on May 19, 2013

Unit 2, RCIC high-energy line break barrier door on May 20, 2013

Unit 1, Core spray topping pump 122 bearing cooling water flow on June 11, 2013

Unit 2, Elevated drywell floor drain leakage on June 11, 2013

Unit 1, Elevated drywell floor drain leakage on June 25, 2013

The inspectors selected these issues based on the risk significance of the associated

components and systems. The inspectors evaluated the technical adequacy of the

operability determinations to assess whether TS operability was properly justified and

the subject component or system remained available such that no unrecognized

increase in risk occurred. The inspectors compared the operability and design criteria in

the appropriate sections of the TSs and UFSAR to CENGs evaluations to determine

whether the components or systems were operable. Where compensatory measures

were required to maintain operability, the inspectors determined whether the measures

in place would function as intended and were properly controlled by CENG. The

inspectors determined, where appropriate, compliance with bounding limitations

associated with the evaluations.

Enclosure

15

b. Findings

No findings were identified.

1R18 Plant Modifications (71111.18 - 3 samples)

.1 Temporary Modifications (1 sample)

a. Inspection Scope

The inspectors reviewed a temporary change to ventilation damper 2HVP*AOD5A which

supplies outside air to the Division III diesel generator room. The inspectors reviewed

10 CFR 50.59 documentation and conducted a field walkdown of the modification to

verify that the temporary modification did not degrade the design bases, licensing bases,

and performance capability of the affected systems.

b. Findings

No findings were identified.

.2 Permanent Modifications (2 samples)

a. Inspection Scope

The inspectors evaluated the following modifications:

Engineering Change Package (ECP) 12-00616 - Installation of a damper for Unit 1

downstream of BV-210-25

ECP 13-000167 - Installation of replacement pump for Unit 1 service water radiation

monitor

The inspectors verified that the design bases, licensing bases, and performance

capability of the affected system was not degraded by the modifications. In addition, the

inspectors reviewed modification documents associated with the upgrade and design

change including the post-installation test procedure, the 10 CFR 50.59 screening form,

and the operational impact assessment form.

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing (71111.19 - 5 samples)

a. Inspection Scope

The inspectors reviewed the post-maintenance tests for the maintenance activities listed

below to verify that procedures and test activities ensured system operability and

functional capability. The inspectors reviewed the test procedure to verify that the

procedure adequately tested the safety functions that may have been affected by the

maintenance activity, that the acceptance criteria in the procedure was consistent with

Enclosure

16

the information in the applicable licensing basis and/or design basis documents, and that

the procedure had been properly reviewed and approved. The inspectors also

witnessed the test or reviewed test data to verify that the test results adequately

demonstrated restoration of the affected safety functions.

Unit 1, Control room ventilation/smoke purge system test following installation of fire

damper BV-21-036 on April 3, 2013

Unit 1, Power board 102 following National Fire Protection Act 805 modification on

April 28, 2013

Unit 1, Isolation valve IV-39-10R following control circuit stop relay replacement on

May 9, 2013

Unit 1, Replacement of excess flow check valve CKV-32-138 on May 10, 2013

Unit 1, IV-29-07R diagnostic testing following body-to-bonnet seal replacement on

May 23, 2013

b. Findings

No findings were identified.

1R20 Refueling and Other Outage Activities (71111.20 - 1 sample)

a. Inspection Scope

The inspectors reviewed the stations work schedule and outage risk plan for the Unit 1

maintenance and refueling outage (N1R22) which was conducted April 14 through May

15, 2013. The inspectors reviewed CENGs development and implementation of outage

plans and schedules to verify that risk, industry experience, previous site-specific

problems, and defense-in-depth were considered. During the outage, the inspectors

observed portions of the shutdown and cooldown processes and monitored controls

associated with the following outage activities:

Configuration management, including maintenance of defense-in-depth,

commensurate with the outage plan for the key safety functions and compliance with

the applicable TSs when taking equipment out of service

Implementation of clearance activities and confirmation that tags were properly hung

and that equipment was appropriately configured to safely support the associated

work or testing

Installation and configuration of reactor coolant pressure, level, and temperature

instruments to provide accurate indication and instrument error accounting

Status and configuration of electrical systems and switchyard activities to ensure that

TSs were met

Monitoring of decay heat removal operations

Impact of outage work on the ability of the operators to operate the SFP cooling

system

Reactor water inventory controls, including flow paths, configurations, alternative

means for inventory additions, and controls to prevent inventory loss

Activities that could affect reactivity

Maintenance of secondary containment as required by TSs

Refueling activities

Fatigue management

Enclosure

17

Tracking of startup prerequisites, walkdown of the drywell (primary containment) to

verify that debris had not been left which could block the emergency core cooling

system suction strainers, and startup and ascension to full power

Identification and resolution of problems related to refueling activities

b. Findings

No findings were identified.

1R22 Surveillance Testing (71111.22 - 8 samples)

a. Inspection Scope

The inspectors observed performance of surveillance tests and/or reviewed test data of

selected risk-significant SSCs to assess whether test results satisfied TSs, the UFSAR,

and CENG procedure requirements. The inspectors verified that test acceptance criteria

were clear, tests demonstrated operational readiness and were consistent with design

documentation, test instrumentation had current calibrations and the range and accuracy

for the application, tests were performed as written, and applicable test prerequisites

were satisfied. Upon test completion, the inspectors considered whether the test results

supported that equipment was capable of performing the required safety functions. The

inspectors reviewed the following surveillance tests:

N1-ST-Q3, Unit 1, High-Pressure Coolant Injection Pump and Check Valve

Operability Test for Train 12 on April 1, 2013

N1-ST-C5, Unit 1, Secondary Containment and Reactor Building Emergency

Ventilation System Operability Test for Loop 11 on April 8, 2013

N1-ISP-LRT-TYC, Unit 1, Local Leak Rate Test for Valves IV-201-09 and IV-201-10

on April 9, 2013

N2-ISP-LDS-Q010, Unit 2, Reactor Building General Area Temperature Instrument

Channel Functional Test on April 18, 2013

Unit 2, RCS Leakage Determination Surveillance and Calculations on April 24, 2013

N2-CSP-GEN-D100, Unit 2, Reactor Water/Auxiliary Water Chemistry Surveillance

on April 24, 2013

N1-TSP-201-001, Unit 1, Integrated Leak Rate Test of Primary Containment Type A

Test on May 8, 2013

N1-ST-Q15, Unit 1, Condensate Transfer System Operability Test on May 30, 2013

b. Findings

Introduction. A self-revealing Green NCV of TS 5.4.1, Procedures, was identified at

Unit 2 when a CENG I&C technician did not properly implement procedure N2-ISP-LDS-

Q010, Reactor Building General Area Temperature Instrument Channel Functional

Test, Revision 00102. As a result, a RHR/RCIC isolation bypass switch was

inadvertently left in the NORMAL position during surveillance testing resulting in an

unplanned RCIC isolation.

Description. The RCIC system is designed to provide adequate makeup water to the

reactor pressure vessel (RPV) automatically or manually following an RPV isolation

accompanied by a loss of coolant flow from the feedwater system. In the event the

Enclosure

18

steam piping to the RCIC pump system leaks, temperature sensors in the RCIC pump

room will close isolation valves in the RCIC system stopping the leak. CENG

surveillance procedure N2-ISP-LDS-Q010 is a TS surveillance test that verifies that the

group 5 (RHR) and group 10 (RCIC) isolation trip signals will close the respective

system isolation valves if a high-temperature condition occurs. The procedure tests this

function by simulating a high temperature condition and verifying correct system

response. Actual valve movement during testing is prevented by control room operators

blocking the test signal.

On April 2, 2013, an unplanned RCIC isolation occurred when I&C technicians did not

properly implement procedure N2-ISP-LDS-Q010 to block the test signal. Specifically,

step 7.2.1 required I&C technicians to request control room operators to place channel

bypass switch E31A-S4B RHR/RCIC ISOLATION BYPASS in BYPASS and to verify the

circuit was bypassed by observing annunciator and plant computer alarms prior to lifting

thermocouple leads in the field. This was not accomplished which resulted in the

isolation of the RCIC system.

Prior to the event, a pre-job brief was conducted by CENG I&C technicians performing

the work which focused on the roles and responsibilities of personnel including the lifting

of thermocouple leads safely and error free. Placing the RHR/RCIC isolation bypass

switch in BYPASS was not identified as a critical step, and no critical steps were

annotated in the work document as required by CNG-PR-1.01-1009, Procedure and

Work Order Use and Adherence Requirements, Revision 00701. However, the

requirement for operations personnel to place the isolation switch in BYPASS was

discussed during the procedure review with the control room supervisor who assigned a

control room operator to perform the task when requested by I&C technicians. Section

3.12 of CNG-PR-1.01-1009 defines place-keeping as physically marking steps to

prevent the omission or duplication of the steps to maintain an accounting of steps in

progress, steps completed, steps not applicable, and steps not yet performed. It lists

among high-risk practices to be avoided by signing or checking off a step as completed

before it is completed. After commencing surveillance procedure N2-ISP-LDS-Q010,

technicians used improper self-checking and place-keeping by checking and initialing as

complete step 7.2.1 to request operators to place the RHR/RCIC isolation bypass switch

in BYPASS and to verify annunciator and computer alarm points were in alarm without

that step having been performed. Consequently, when thermocouple leads were lifted in

the following step, a false high-temperature signal was generated resulting in the closing

of RCIC steam supply isolation valves 2ICS*MOV121, 2ICS*MOV128, 2ICS*MOV170,

and an unplanned isolation of RCIC. The surveillance test was immediately stopped, the

required TS action statements were entered for the RCIC system, and the system was

restored to an operable status after approximately 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. The isolation signal was also

sent to the RHR system for SDC supply and return valves and for reactor head spray

isolation valve which were already closed at power. There was no impact on operability

of low-pressure coolant injection or containment spray functions of RHR.

A CENG investigation concluded human error as the primary cause for the inadvertent

isolation of the RCIC system. A contributing cause was the failure to implement

adequate corrective actions following a similar RCIC isolation event in 2007. Immediate

corrective actions for this event included a human performance stand down that

reinforced use of human performance tools and the need to identify and mark critical

steps during pre-job briefs, retraining the I&C technicians involved in the event on proper

use of human performance error prevention techniques, and improving bypass switch

Enclosure

19

verification steps for procedure N2-ISP-LDS-Q010 and other similar leak detection

system surveillance procedures. CENG entered this issue in their CAP as CR-2013-

002461.

Analysis. The inspectors determined that CENGs failure to correctly implement

surveillance test procedure N2-ISP-LDS-Q010 was a performance deficiency that was

within CENGs ability to foresee and correct and should have been prevented. This

finding is more than minor because it is associated with the human performance attribute

of the Mitigating Systems cornerstone and affected the cornerstone objective to ensure

the availability, reliability, and capability of systems that respond to initiating events to

prevent undesirable consequences (i.e., core damage). Specifically, the inadvertent

isolation rendered the RCIC system inoperable and unable to perform its function for

approximately 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. Additionally, this finding is similar to Example 4.b. of IMC 0612,

Appendix E, Examples of Minor Issues, and is more than minor due to the procedural

error leading to a plant transient, i.e. an unplanned RCIC isolation.

In accordance with IMC 0609.04, Initial Characterization of Findings, and Exhibit 2 of

IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power,

issued June 19, 2012, this finding represents a loss of safety function. Unit 2 is a

BWR-5, and as a result, RCIC is treated as having a separate high- pressure injection

safety function. A detailed analysis was conducted using SAPHIRE Version 8.0.8.0 and

Unit 2 SPAR Model 8.17. Using an exposure period of 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and conservatively

assuming no recovery of the failed equipment, this finding had a change in core damage

frequency of low E-8. The dominant accident sequence was a grid- related loss of off-

site power with a failure of Division III power and the failure to recover off-site power and

the EDGs in 30 minutes. Since the change in core damage frequency was less than

1E-7, contributions from large early release and external event did not need to be

considered. Therefore, this finding was determined to be of very low safety significance

(Green).

This finding had a cross-cutting aspect in the area of Human Performance, Work

Practices, because the I&C technicians did not effectively employ self-checking and

place-keeping when implementing N2-ISP-LDS-Q010 which directly contributed to the

resulting procedural error H.4(a).

Enforcement. TS 5.4.1, Procedures, requires written procedures to be established,

implemented, and maintained covering the applicable procedures recommended in

Regulatory Guide (RG) 1.33, Quality Assurance Program Requirements (Operation),

Appendix A, Revision 2, dated February 1978. Section 8.b(2)(b) of RG 1.33 requires, in

part, specific procedures for surveillance tests on containment isolation. CENG

surveillance test procedure N2-ISP-LDS-Q010, Reactor Building General Area

Temperature Instrument Channel Functional Test, directed that the RHR/RCIC

ISOLATION BYPASS switch be placed in BYPASS to prevent an inadvertent

containment isolation while lifting thermocouple leads. Contrary to above, on April 2,

2013, technicians lifted thermocouple leads without ensuring the isolation switch was

bypassed, resulting in an unplanned isolation of the RCIC system. Because this issue is

of very low safety significance (Green) and was entered into CENGs CAP as CR-2013-

002461, this violation is being treated as an NCV, consistent with Section 2.3.2 of the

NRC Enforcement Policy. (NCV 05000410/2013003-01, Failure to Follow

Containment Isolation System Surveillance Procedure Resulting in Isolation of the

Reactor Coolant Isolation Cooling System)

Enclosure

20

Cornerstone: Emergency Preparedness

1EP4 Emergency Action Level and Emergency Plan Changes (71114.04 - 1 sample)

a. Inspection Scope

The Office of Nuclear Security and Incident Response headquarters staff performed an

in-office review of the latest revisions of various emergency plan implementing

procedures and the emergency plan located under ADAMS accession number

ML131071146 as listed in the Attachment.

CENG determined that in accordance with 10 CFR 50.54(q), the changes made in the

revisions resulted in no reduction in the effectiveness of the plan and that the revised

plan continued to meet the requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR

Part 50. The NRC review was not documented in a safety evaluation report and did not

constitute approval of CENG-generated changes; therefore, this revision is subject to

future inspection.

b. Findings

No findings were identified.

1EP6 Drill Evaluation (71114.06 - 1 sample)

Training Observation

a. Inspection Scope

The inspectors observed a simulator training evolution for CENGs licensed operators on

April 2, 2013, which required emergency plan implementation by an operations crew.

The inspectors observed Unit 1 licensed operator performance during an evaluated

simulator scenario that included a loss of condenser vacuum, a stuck open ERV, and an

anticipated transient without scram. CENG planned for this evolution to be evaluated

and included in performance indicator data regarding drill and exercise performance.

The inspectors observed event classification and notification activities performed by the

crew. The focus of the inspectors activities was to note any weaknesses and

deficiencies in the crews performance and ensure that CENG evaluators noted the

same issues and entered them into the CAP.

b. Findings

No findings were identified.

Enclosure

21

2. RADIATION SAFETY

Cornerstone: Public Radiation Safety and Occupational Radiation Safety

2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01)

a. Inspection Scope

From April 22 to 25, 2013, the inspectors reviewed and assessed CENGs performance

in assessing the radiological hazards and exposure control in the workplace associated

with licensed activities and the implementation of appropriate monitoring and exposure

control measures for both individual and collective exposures.

The inspectors interviewed the radiation protection manager, radiation protection

supervisors, radiation protection technicians (RPTs), and radiation workers. The

inspectors performed walkdowns of various portions of the plant, performed independent

radiation dose rate measurements, observed work activities in radiological control areas,

and reviewed CENG documents during the N1R22 outage. The inspectors used the

requirements in 10 CFR 20, guidance in Regulatory Guide (RG) 8.38, Control of Access

to High and Very High Radiation Areas of Nuclear Plants, TSs, and CENGs procedures

required by TSs as criteria for determining compliance.

Inspection Planning

The inspectors reviewed the results of radiation protection program audits. The

inspectors reviewed reports of operational occurrences related to occupational radiation

safety since the last inspection on March 21, 2013.

Radiological Hazard Assessment

The inspectors conducted walkdowns and independent radiation measurements to

evaluate material, work and radiological conditions in the facility including the drywell,

RB, refueling floor, and turbine building (TB).

The inspectors selected the following radiological risk-significant work activities that

involved exposure to radiation:

Refueling floor activities

Drywell control rod drive under-vessel work

Drywell scaffolding

Drywell ISI

RWCU valve repairs

For these work activities, the inspectors assessed whether the pre-work surveys

performed were appropriate to identify and quantify the radiological hazard and to

establish adequate protective measures. The inspectors evaluated the radiological

survey program to determine if radiological hazards were properly identified.

The inspectors observed work in potential airborne radioactivity areas and evaluated

whether the air samples from under the reactor vessel, from the reactor cavity and for

Enclosure

22

entries into the tent for repair of the SFP gate, were representative of the breathing air

zone and were properly evaluated. The inspectors evaluated whether continuous air

monitors on the refueling floor in the RB and at the drywell entrance were located to

ensure appropriate detection sensitivity and were representative of actual work areas.

The inspectors evaluated CENGs program for monitoring levels of loose surface

contamination in areas of the plant.

Instructions to Workers

The inspectors reviewed the following radiation work permits (RWPs) used to access

high radiation areas and evaluated if the specified work control instructions and control

barriers were consistent with TS requirements for locked high radiation areas:

RWP 113330H, RB 261 RWCU Valve Work

RWP 113802H, Drywell Under-Vessel Work

RWP 113890A, RB 340 Reactor Disassembly and Reassembly

RWP 113890B, RB 340 Underwater Work on Refuel Floor

RWP 113890E, RB 340 Reactor Cavity and Equipment Storage Pit Decon

RWP 113806H, Drywell ISI

RWP 113815, RB 261 Flow Accelerated Corrosion (FAC) ISI

RWP 113810, Drywell General Scaffolding Activities

The inspectors assessed whether permissible dose for radiological-significant work

under each RWP was clearly identified. The inspectors evaluated whether electronic

personal dosimeter alarm set points were in conformance with survey indications and

plant procedural requirements.

The inspectors reviewed CR-2013-002474 and CR-2012-002974 for occurrences where

a workers electronic personal dosimeter noticeably malfunctioned or alarmed. The

inspectors evaluated whether workers responded appropriately to the off-normal

condition. The inspectors assessed whether the issue was included in the CAP and

whether compensatory dose evaluations were conducted.

For work activities that could suddenly and severely increase radiological conditions, i.e.,

upper elevation of drywell during spent fuel movement and low power range monitor

moves, the inspectors assessed CENGs means to inform workers of these changes that

could significantly impact their occupational dose.

Contamination and Radioactive Material Control

The inspectors observed the access control point where CENG monitors potentially

contaminated material leaving the radiological control area and inspected the methods

used for control, survey, and release from these areas. The inspectors observed the

performance of personnel surveying and releasing material for unrestricted use and

evaluated whether the release surveys were performed in accordance with plant

procedures and process knowledge concerning the equipment.

Enclosure

23

Radiological Hazards Control and Work Coverage

The inspectors evaluated ambient radiological conditions and performed independent

radiation measurements during plant walkdowns. The inspectors assessed whether the

conditions were consistent with applicable posted surveys, RWPs, and associated

worker briefings.

The inspectors assessed whether radiation monitoring devices were placed on the

individuals body consistent with CENG procedures. The inspectors assessed whether

the dosimeter was placed in the location of highest expected dose and that CENG

properly implemented an NRC-approved method of determining effective dose

equivalent.

The inspectors reviewed the application of dosimetry to effectively monitor exposure to

personnel in high radiation work areas with significant dose rate gradients; e.g., RWCU

repairs and workers under vessel in the control rod drive area.

The inspectors reviewed the following RWPs for work within airborne radioactivity areas

with the potential for individual worker internal exposures:

RWP 113802H, Under-Vessel Control Rod Drive Work

RWP 113330H, RWCU Valve Work

RWP 113890E, RB 340 Reactor Cavity and Equipment Storage Pit Decontamination

The inspectors evaluated airborne radioactive controls and monitoring including potential

for significant airborne levels. The inspectors assessed applicable containment barriers

integrity and the operation of temporary high-efficiency particulate air ventilation system.

Risk-Significant High Radiation Area and Very High Radiation Area Controls

The inspectors discussed the controls and procedures for high risk high radiation areas

and very high radiation areas with the radiation protection manager. The inspectors

discussed with first-line health physics supervisors the controls in place for special areas

that have the potential to become very high radiation areas during refueling outages.

The inspectors evaluated the controls for very high radiation areas and areas with the

potential to become a very high radiation area to ensure that an individual was not able

to gain unauthorized access to these areas.

Radiation Worker Performance

The inspectors observed the performance of radiation workers during the N1R22 with

respect to stated radiation protection work requirements. The inspectors assessed

whether workers were aware of the radiological conditions in their workplace, the RWP

controls and limits, and whether their behavior reflected the level of radiological hazards

present.

Radiation Protection Technician Proficiency

The inspectors observed the performance of the RPTs during the N1R22 with respect to

controlling radiation work. The inspectors evaluated whether technicians were aware of

Enclosure

24

the radiological conditions in their workplace, the RWP controls and limits, and whether

their behavior was consistent with their training and qualifications with respect to the

radiological hazards and work activities.

Problem Identification and Resolution

The inspectors evaluated whether problems associated with radiation monitoring and

exposure control were being identified by CENG at an appropriate threshold and were

properly addressed for resolution in the CENGs CAP. The inspectors assessed the

appropriateness of the corrective actions for a selected sample of problems documented

by CENG that involved radiation monitoring and exposure controls. The inspectors

assessed CENGs process for applying operating experience to their plant.

b. Findings

No findings were identified.

2RS2 Occupational ALARA Planning and Controls (71124.02)

a. Inspection Scope

The inspectors assessed performance with respect to maintaining occupational

individual and collective radiation exposures as low as reasonably achievable (ALARA)

during the N1R22. The inspectors used the requirements in 10 CFR 20, RG 8.8,

Information Relevant to Ensuring that Occupational Radiation Exposures at Nuclear

Power Stations will be As Low As Is Reasonably Achievable, RG 8.10, Operating

Philosophy for Maintaining Occupational Radiation Exposures As Low As Is Reasonably

Achievable, TSs, and CENGs procedures required by TSs as criteria for determining

compliance.

Inspection Planning

The inspectors reviewed pertinent information regarding CENGs collective dose history,

current exposure trends, and ongoing or planned activities in order to assess current

performance and exposure challenges.

The inspectors reviewed changes in the radioactive source term by reviewing the trend

in average contact dose rates on reactor recirculation piping for the time period between

1984 and the present Unit 1 outage. The inspectors reviewed ALARA procedures that

specified the processes used to estimate and track exposures for radiological work

activities.

Radiological Work Planning

The inspectors selected the following work activities that had the highest exposure

significance:

ALARA Plan 2013-1-002, Drywell Under-Vessel Activities and Associated Activities

N1R22

ALARA Plan 2013-1-004, Drywell Operations and Local Leak Rate Test Activities

Enclosure

25

ALARA Plan 2013-1-006, Drywell ISI Activities

ALARA Plan 2013-1-007, Recirculation Pump Seals Replacement and Motor PMs

(Numbers 11, 13, and 15)

ALARA Plan 2013-1-010, Drywell Scaffold Activities

ALARA Plan 2013-1-014, Drywell Emergency Relief Valve and Pilot Valve Work

Activities

ALARA Plan 2013-1-024, Main Steam Isolation Valve 01-02 Stem Replacement

Actuator Remove/Replace and Testing

ALARA Plan 2013-1-029, Balance of Plant FAC Activities in RWCU Heat Exchanger

Room and Valve Aisles

ALARA Plan 2013-1-030, Refuel Floor Activities

ALARA Plan 2013-1-031, RWCU Miscellaneous Maintenance, Preventive

Maintenance, Surveillance Testing, Operations N1R22

The inspectors reviewed the ALARA work activity evaluations, exposure estimates, and

exposure reduction requirements. The inspectors determined whether CENG

reasonably grouped the radiological work into work activities based on historical

precedence, industry norms, and/or special circumstances.

The inspectors assessed when CENGs planning identified appropriate dose reduction

techniques, considered alternate dose reduction features, and estimated reasonable

dose goals. The inspectors evaluated whether the ALARA assessment had taken into

account decreased worker efficiency from use of respiratory protective devices and/or

heat stress mitigation equipment. The inspectors determined whether work planning

considered the use of remote technologies as a means to reduce dose and the use of

dose reduction insights from industry operating experience and plant-specific lessons

learned. The inspectors assessed the integration of ALARA requirements into work

procedure and RWP documents.

Verification of Dose Estimates and Exposure Tracking Systems

The inspectors reviewed the assumptions and basis for the current annual collective

dose estimate and outage collective dose estimate for accuracy. The inspectors

reviewed applicable procedures to determine the methodology for estimating exposures

from specific work activities and for department and station collective dose goals.

The inspectors evaluated whether CENG had established measures to track, trend, and

reduce occupational doses for ongoing work activities. The inspectors assessed

whether dose threshold criteria were established to prompt additional reviews and/or

additional ALARA planning and controls.

The inspectors evaluated CENGs method of adjusting exposure estimates or

re-planning work when unexpected changes in scope or emergent work were

encountered. The inspectors assessed whether adjustments to exposure estimates

were based on sound radiation protection and ALARA principles or if they were just

adjusted to account for failures to plan/control the work.

Enclosure

26

Source Term Reduction and Control

The inspectors used station records to determine the historical trends and current status

of plant source term known to contribute to elevated facility collective exposure. The

inspectors assessed whether CENG had made allowances or developed contingency

plans for expected changes in the source term as the result of changes in plant fuel

performance issues or changes in plant primary chemistry.

Radiation Worker Performance

The inspectors observed radiation workers and RPTs performance during refueling

outage activities in radiation areas, airborne radioactivity areas, and high radiation areas.

The inspectors evaluated whether workers demonstrated the ALARA philosophy in

practice and whether there were any procedure or RWP compliance issues.

Problem Identification and Resolution

The inspectors evaluated whether problems associated with ALARA planning and

controls were being identified by CENG at an appropriate threshold and were properly

addressed for resolution in the CENGs CAP.

b. Findings

No findings were identified.

2RS3 In-Plant Airborne Radioactivity Control and Mitigation (71124.03)

a. Inspection Scope

This area was inspected to verify in-plant airborne concentrations were being controlled

consistent with ALARA principles and the use of respiratory protection devices on-site

does not pose an undue risk to the wearer. The inspectors used the requirements in

10 CFR 20, the guidance in RG 8.15, Acceptable Programs for Respiratory Protection,

RG 8.25, Air Sampling in the Workplace, NUREG-0041, Manual of Respiratory

Protection Against Airborne Radioactive Material, TSs, and CENGs procedures

required by TSs as criteria for determining compliance.

Inspection Planning

The inspectors reviewed the UFSAR to identify areas of the plant designed as potential

airborne radiation areas and any associated ventilation systems or airborne monitoring

instrumentation. This review included instruments used to identify changing airborne

radiological conditions such that actions to prevent an overexposure may be taken. The

review included an overview of the respiratory protection program and a description of

the types of devices used. The inspectors reviewed procedures for maintenance,

inspection, and use of respiratory protection equipment as well as procedures for

maintenance and testing of breathing air quality.

Enclosure

27

Engineering Controls

The inspectors reviewed CENGs use of permanent and temporary ventilation to

determine whether CENG uses ventilation systems as part of its engineering controls to

control airborne radioactivity. The inspectors reviewed procedural guidance for use of

installed plant systems to reduce dose and assessed whether the systems are used

during high-risk activities.

The inspectors selected two temporary ventilation system setups on the refuel floor used

to support work in contaminated areas. The inspectors assessed whether the use of

these systems is consistent with procedural guidance and ALARA principles.

The inspectors reviewed airborne monitoring protocols for the drywell and refueling floor

continuous air monitors used to monitor and warn of changing airborne concentrations in

the plant and evaluating whether the alarms and set points are sufficient to prompt

worker action to ensure that doses are maintained within the limits of 10 CFR 20 and the

ALARA concept.

The inspectors assessed whether CENG had established threshold criteria for

evaluating levels of airborne beta-emitting and alpha-emitting radionuclides.

Use of Respiratory Protection Devices

The inspectors selected RWCU repairs and under-vessel control rod drive work activities

where respiratory protection devices were used to limit the intake of radioactive

materials and assessed whether CENG performed an evaluation concluding that further

engineering controls were not practical and that the use of respirators is ALARA. The

inspectors also evaluated whether CENG had established means (such as routine

bioassay) to determine if the level of protection (protection factor) provided by the

respiratory protection devices during use was at least as good as that assumed in work

controls and dose assessment.

Problem Identification and Resolution

The inspectors evaluated whether problems associated with the control and mitigation of

in-plant airborne radioactivity were being identified by CENG at an appropriate threshold

and were properly addressed for resolution in CENGs CAP. The inspectors assessed

whether the corrective actions were appropriate for a selected sample of problems

involving airborne radioactivity and were appropriately documented.

b. Findings

No findings were identified.

2RS4 Occupational Dose Assessment (71124.04)

a. Inspection Scope

From April 22 to 25, 2013, the inspectors reviewed occupational doses to ensure they

were appropriately monitored and assessed. The inspectors used the requirements in

10 CFR 20, RG 8.13, Instruction Concerning Prenatal Radiation Exposure, RG 8.36,

Enclosure

28

Radiation Dose to the Embryo/Fetus, RG 8.40, Methods for Measuring Effective Dose

Equivalent from External Exposure, TSs, and CENGs procedures required by TSs as

criteria for determining compliance.

Inspection Planning

The inspectors reviewed the results of Unit 1 radiation protection program audits related

to internal and external dosimetry. A review was conducted of procedures associated

with dosimetry operations including issuance/use of external dosimetry, assessment of

internal dose, and evaluation of and dose assessment for radiological incidents. The

inspectors evaluated whether CENG had established procedural requirements for

determining when external dosimetry and internal dose assessments are required.

External Dosimetry

The inspectors evaluated whether CENGs dosimetry vendor was accredited with the

National Voluntary Laboratory Accredited Program and if the approved irradiation test

categories for each type of personnel dosimeter used were consistent with the types and

energies of the radiation present and the way the dosimeter is being used.

The inspectors evaluated the onsite storage of dosimeters before issuance, during use,

and before processing and reading. The inspectors also reviewed the guidance

provided to radiation workers with respect to care and storage of dosimeters.

The inspectors assessed the use of electronic personal dosimeters to determine if

CENG uses a correction factor to address the response of the electronic personal

dosimeter as compared to the dosimeter of legal record for situations when the

electronic personal dosimeter is used to assign dose and whether the correction factor is

based on sound technical principles.

The inspectors reviewed two CAP documents for adverse trends related to electronic

personal dosimeters. The inspectors assessed whether CENG had identified any

adverse trends and implemented appropriate corrective actions.

Internal Dosimetry

Routine Bioassay (In Vivo)

The inspectors reviewed procedures used to assess the dose from internally deposited

radionuclides using whole body counting equipment. The inspectors evaluated whether

the procedures addressed methods for differentiating between internal and external

contamination, the release of contaminated individuals, determining the route of intake

and the assignment of dose.

The inspectors reviewed CENGs evaluation for use of its portal radiation monitors as a

passive monitoring system. The inspectors assessed if instrument minimum detectable

activities were adequate to determine the potential for internally deposited radionuclides

sufficient to prompt an investigation.

Enclosure

29

Special Bioassay (In Vitro)

There was no internal dose assessments obtained using whole body count results for

the inspectors to review. There was no internal dose assessments obtained using

urinalysis or fecal sample results for the inspectors to review.

The inspectors reviewed the vendor laboratory quality assurance program and assessed

whether the laboratory participated in an industry-recognized cross check program

including whether out-of-tolerance results were reviewed, evaluated, and resolved

appropriately.

Internal Dose Assessment - Airborne Monitoring

The inspectors reviewed CENGs program for dose assessment based on airborne

monitoring and calculations of derived air concentration calculations. The inspectors

determined whether flow rates and collection times for air sampling equipment were

adequate to allow appropriate lower limits of detection to be obtained. CENG had

performed internal dose assessments using airborne/derived air concentration

monitoring for some work in the cavity during the N1R22.

Internal Dose Assessment - Whole Body Count Analyses

CENG has not documented any internal dose assessments using whole body count

results during the period reviewed.

Special Dosimetry Situations

Declared Pregnant Workers

The inspectors assessed the process used by CENG to inform workers of the risks of

radiation exposure to the embryo/fetus, the regulatory aspects of declaring a pregnancy,

and the specific process to be used for monitoring and controlling exposure to a

declared pregnant worker. CENG has not documented any internal dose assessments

for declared pregnant workers during this inspection period.

Dosimeter Placement and Assessment of Effective Dose Equivalent for External

Exposures

The inspectors reviewed CENGs methodology for monitoring external dose in non-

uniform radiation fields or where large dose gradients exist. The inspectors evaluated

CENGs criteria for determining when alternate monitoring such as use of multi-badging

is to be implemented.

The inspectors reviewed dose assessments performed for workers performing under-

vessel work and RWCU repairs. These workers used multi-badging to evaluate effective

dose equivalent and the dose assessment was performed consistent with CENG

procedures and dosimetry standards.

Enclosure

30

Shallow Dose Equivalent

There were no dose assessments for shallow dose equivalent available for review. The

inspectors evaluated CENGs method for calculating shallow dose equivalent from

distributed skin contamination or discrete radioactive particles.

Assigning Dose of Record

For the special dosimetry situations reviewed in this section, the inspectors assessed

how CENG assigns dose of record for total effective dose equivalent, shallow dose

equivalent, and lens dose equivalent. This included an assessment of external and

internal monitoring results, supplementary information on individual exposures, and

radiation surveys when dose assessment was based on these techniques.

Problem Identification and Resolution

The inspectors assessed whether problems associated with occupational dose

assessment are being identified by CENG at an appropriate threshold and are properly

being addressed for resolution in CENGs CAP. The inspectors assessed the

appropriateness of the corrective actions for a selected sample of problems documented

by CENG involving occupational dose assessment.

b. Findings

No findings were identified.

2RS7 Radiological Environmental Monitoring Program (71124.07)

a. Inspection Scope

From May 6 to 10, 2013, the inspectors verified that the radiological environmental

monitoring program (REMP) quantifies the impact of radioactive effluent released to the

environment and sufficiently validates the integrity of the radioactive gaseous and liquid

effluent release program.

The inspectors used the requirements in 10 CFR 20; 10 CFR 50, Appendix A, Criterion

60, Control of Release of Radioactivity to the Environment; 10 CFR 50, Appendix I,

Numerical Guides for Design Objectives and Limiting Conditions for Operations to Meet

the Criterion As Low As Is Reasonably Achievable for Radioactive Material in Light-

Water-Cooled Nuclear Power Reactor Effluents; 40 CFR 190, Environmental Radiation

Protection Standards for Nuclear Power Operations; 40 CFR 141, Maximum

Contaminant Levels for Radionuclides; RG 1.23, Meteorological Monitoring Programs

for Nuclear Power Plants; RG 4.1, Radiological Environmental Monitoring for Nuclear

Power Plants; RG 4.15, Quality Assurance for Radiological Monitoring Programs;

NUREG-1302, Offsite Dose Calculation Manual Guidance: Standard Radiological

Effluent Controls for Boiling Water Reactors; applicable industry standards; and CENG

procedures as criteria for determining compliance.

Enclosure

31

Inspection Planning

The inspectors reviewed CENGs annual radiological environmental operating reports for

2011 and 2012 and the results of any assessments since the last inspection to verify that

the REMP was implemented and reported in accordance with requirements. This review

included changes to the offsite dose calculation manual (ODCM) in environmental

monitoring, sampling locations, monitoring and measurement frequencies, land-use

census, inter-laboratory comparison program, and analysis of environmental data.

The inspectors reviewed Units 1 and 2 ODCMs to identify locations of environmental

monitoring stations. The inspectors reviewed Units 1 and 2 UFSARs for information

regarding the environmental monitoring program and meteorological monitoring

instrumentation. The inspectors reviewed quality assurance audits and technical

evaluations performed on the vendor analytical laboratory program.

The inspectors reviewed Units 1 and 2 radioactive effluent release reports for 2011 and

2012 and the most recent results from waste stream analysis to determine if CENG was

sampling and analyzing for the predominant radionuclides released in plant effluents.

Site Environmental Inspection

The inspectors walked down five air sampling stations and five environmental thermo

luminescent dosimeter (TLD) monitoring stations to determine whether they were

located as described in the ODCM and to determine the equipment material condition.

For the air samplers and TLD stations selected, the inspectors reviewed the calibration

and maintenance records to verify that they demonstrated adequate operability for these

components. Additionally, the review included the calibration and maintenance records

of four composite water samplers.

The inspectors performed an assessment of any compensatory environmental sampling

upon loss of a required sampling station.

The inspectors observed the collection and preparation of four environmental samples

from surface water and fish to verify that environmental sampling was representative of

the effluent release pathways as specified in the ODCM and that sampling techniques

were in accordance with procedures.

Based on direct observation and review of records, the inspectors assessed whether the

meteorological instruments were operable, calibrated, and maintained in accordance

with procedures. The inspectors assessed whether the meteorological data readout and

recording instruments in the control room and at the meteorological tower were operable

and accurate.

The inspectors evaluated whether missed and/or anomalous environmental samples

were identified and reported in the annual radiological environmental operating reports.

The inspectors selected five events that involved a missed sample or inoperable sampler

to verify that CENG had identified the cause and had implemented corrective actions.

The inspectors reviewed the assessment of any sample results detected above the

lower limits of detection and reviewed CENGs evaluation of associated radioactive

effluent release data that was the potential source of the released material. The 2011

Enclosure

32

radiological environmental operator report noted the detection of Iodine from the

Fukushima Daiichi accident during March and April 2011.

The inspectors selected the following five SSCs that contained licensed material for

which there was a credible mechanism for radioactive material to reach ground water:

Unit 1 drywell, reactor, and turbine building sumps

Unit 2 drywell, reactor, and turbine building sumps

Unit 2 stack condensate transfer line to radwaste

Old radwaste sumps W 11, 12, and 13, and concentrator waste tank cubicle

Waste water treatment facility clarified tanks and sludge pits

The inspectors assessed whether CENG had implemented a sampling, inspection, and

monitoring program to provide early detection of leakage from these SSCs to ground

water.

The inspectors evaluated whether decommissioning records of leaks, spills, and

environmental remediation since the previous inspection were retained in a retrievable

manner in the 10 CFR 50.75(g) decommissioning file. Two records were added to the

decommissioning file in 2012. The first was Unit 1 turbine building roof replacement,

and the second was tritium in-leakage to the Unit 1 screen house.

The inspectors reviewed any significant changes made by CENG to the ODCM as the

result of changes to the land census, long-term meteorological conditions, or

modifications to the sampler stations since the last inspection. The inspectors reviewed

technical justifications for any changed sampling locations to ensure that the changes

did not affect CENGs ability to monitor the impact of plant operations on the

environment.

The inspectors assessed whether the detection sensitivities for environmental samples

were below the lower limits of detection specified in the ODCM. The inspectors

reviewed quality control charts for laboratory radiation measurement instrument and

actions taken for degrading detector performance. The inspectors also reviewed the

results of the vendors quality control program including the inter-laboratory comparison

to assess the adequacy of the vendors program.

The inspectors reviewed the results of Entergy Nuclear Northeast (Entergy) inter-

laboratory and intra-laboratory comparison program to verify the adequacy of

environmental sample analyses performed by James A. Fitzpatrick Nuclear Power Plant

environmental laboratory. The inspectors assessed whether the results included for the

media radionuclide mix was appropriate for the facility.

Identification and Resolution of Problems

The inspectors assessed whether problems associated with the REMP and

meteorological monitoring programs were being identified by CENG at an appropriate

threshold and correction actions were assigned for resolution in CENGs CAP.

Enclosure

33

b. Findings

No findings were identified.

4. OTHER ACTIVITIES

4OA1 Performance Indicator Verification (71151)

RCS Specific Activity and RCS Leak Rate (4 samples)

a. Inspection Scope

The inspectors reviewed CENGs submittal for the RCS specific activity (BI01) and RCS

leak rate (BI02) performance indicators for both Unit 1 and Unit 2 for the period of April

1, 2011, through March 31, 2013. (Note: An additional 12 months of BI02 data was

reviewed due to CENG having updated and revised the BI02 performance indicator data

since the previous inspection.) To determine the accuracy of the performance indicator

reported during those periods, the inspectors used definitions and guidance contained in

Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance

Indicator Guideline, Revision 6. The inspectors also reviewed RCS sample analysis

and control room logs of daily measurements of RCS leakage and compared that

information to the data reported by the performance indicator. Additionally, the

inspectors observed surveillance activities that determined the RCS identified leakage

rate, and chemistry personnel taking and analyzing an RCS sample.

b. Findings

No findings were identified.

4OA2 Problem Identification and Resolution (71152 - 4 samples)

.1 Routine Review of Problem Identification and Resolution Activities

a. Inspection Scope

As required by Inspection Procedure 71152, Problem Identification and Resolution, the

inspectors routinely reviewed issues during baseline inspection activities and plant

status reviews to verify that CENG entered issues into the CAP at an appropriate

threshold, gave adequate attention to timely corrective actions, and identified and

addressed adverse trends. In order to assist with the identification of repetitive

equipment failures and specific human performance issues for follow-up, the inspectors

performed a daily screening of items entered into the CAP.

b. Findings

No findings were identified.

Enclosure

34

.2 Semi-Annual Trend Review

a. Inspection Scope

The inspectors performed a semi-annual review of site issues, as required by Inspection

Procedure 71152 to identify trends that might indicate the existence of more significant

safety issues. In this review, the inspectors included repetitive or closely related issues

that may have been documented by CENG outside of the CAP such as trend reports,

performance indicators, major equipment problem lists, system health reports,

maintenance rule assessments, and maintenance or CAP backlogs. The inspectors also

reviewed CENGs CAP database for the first and second quarters of 2013 to assess

condition reports written in various subject areas (equipment problems, human

performance issues, etc.) as well as individual issues identified during the NRCs daily

condition report review (Section 4OA2.1). The inspectors reviewed CENGs quarterly

trend report for the first quarter of 2013 conducted under CNG-QL-1.01-1008, Periodic

QPA Performance Reporting Process, Revision 00500, to verify that CENG personnel

were appropriately evaluating and trending adverse conditions in accordance with

applicable procedures.

b. Findings and Observations

No findings were identified.

Two trends were identified by the inspectors that had not been identified by CENG.

The inspectors noted a negative trend in the reliability and availability of the emergency

core cooling system (ECCS) keep-fill pumps on Unit 2. The low-pressure core spray

keep-fill pump 2CLS*P2 failed on January 9, 2013, due to motor overload (CR-2013-

000218). On February 28, the HPCS keep-fill pump suddenly failed (CR-2013-001633).

As part of an extent-of-condition review for the low-pressure core spray keep-fill pump

failing, operators identified that Division II RHR system keep-fill pump 2RHS*P2 motor

had an abnormal noise. On April 12, CENG replaced 2RHS*P2 motor. The ECCS

keep-fill pumps are Goulds Pump Model 3196ST with 215T Westinghouse motors rated

for 575 volts. Westinghouse investigations determined that each motor had a turn-to-

turn failure. The failure of the HPCS keep-fill pump resulted in Licensee Event Report

(LER) 2013-002, Failure of High-Pressure Core Spray System Pressure Pump due to a

Motor Winding Failure, in accordance with 10 CFR Part 50.73(a)(2)(v)(D) and 10 CFR

Part 21. All three keep-fill pump motors have been replaced, and CENG has entered

these issues into their CAP as noted by the condition reports above.

The inspectors noted a decrease in the reliability of the Unit 1 RB sumps, and as a

result, an increase in the number of emergency operating procedure entries by control

room operators due to sump failures. The decrease in reliability was noted by three

separate events regarding Unit 1 RB sumps that resulted in emergency operating

procedure entries. These events occurred on January 20, April 12, and April 24, and

were documented in CR-2013-000532, CR-2013-002743 and CR-2013-003371,

respectively. The inspectors review identified that although CENG had properly

assessed sump performance per the NRC maintenance rule 10 CFR 50.65 for the train

level criteria, CENG did not assess sump performance against the system level criteria.

CENG documented this issue in CR-2013-004828 and entered this issue into their CAP.

A subsequent CENG evaluation determined the RB floor and equipment sumps had

exceeded their performance monitoring group functional failure criteria and the systems

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were placed into (a)(1) status. The inspectors determined that this issue was not more

than minor because the train level criteria were appropriately being monitored and

placing the RB sumps into (a)(1) status for exceeding system level criteria would not

have resulted in additional maintenance-related corrective actions being taken by

CENG.

.3 Annual Sample: Review of Repetitive Valve Packing Leakage Issues

a. Inspection Scope

The inspectors performed an in-depth review of CENGs root cause analysis and

corrective actions associated with CR-2011-007171 and CR-2011-010906 regarding two

forced shutdowns of Unit 2 due to excessive unidentified leak rates in 2011. The

inspectors focused on the implementation of corrective actions and extent-of-condition

and cause reviews as it applied to both units.

The inspectors assessed CENGs problem identification threshold, cause analyses,

extent-of-condition reviews, compensatory actions, and the prioritization and timeliness

of CENGs corrective actions to determine whether CENG was appropriately identifying,

characterizing, and correcting problems associated with this issue and whether the

planned or completed corrective actions were appropriate. The inspectors compared the

actions taken to the requirements of CENGs CAP and 10 CFR 50, Appendix B. In

addition, the inspectors performed field walkdowns and interviewed engineering

personnel to assess the effectiveness of the implemented corrective actions.

b. Findings and Observations

No findings were identified.

On August 6 and December 9, 2011, Unit 2 conducted forced shutdowns due to

excessive unidentified leakage rate. In both cases, the increased unidentified leakage

was determined to be from the failure of the recirculation discharge gate valve,

2RCS*MOV18A. CENG completed separate root cause analysis for both events and

determined the August 6 event was due to a design issue which subjects the packing to

excessive vibrations due to the valve gate being exposed to RCS system flow. The

December 9 event was determined to be the result of a workmanship error following the

August 6 event which resulted in a burr forming on the valve stem and eventually led to

the second packing failure.

The inspectors reviewed the root cause analysis and the ECP associated with the 2001

change in packing design for this valve. The inspectors reviewed photos and drawings

of the valve and interviewed engineering personnel. The inspectors concluded that

CENGs determination of the root cause and major contributing causes were reasonable

and had a sound technical basis. The inspectors also determined that corrective actions

for the August 6 event would not have been expected to preclude the December 9 event.

The inspectors reviewed CENGs extent-of-condition reviews and corrective actions

related to similar valves on both Units 1 and 2. The inspectors concluded that CENG

conducted an appropriate extent-of-condition review and identified other valves which

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may be susceptible to the same failure mechanism. CENG also developed corrective

actions to enhance their valve packing program and designated an engineer to oversee

this program.

The inspectors conducted an independent review of condition reports from 2000 until the

present looking for excessive leakage issues associated with valve packing. The

inspectors confirmed that a large percentage of issues prior to 2001 and since 2007

have been related to RCS*MOV18A and the underlying design vulnerability. Corrective

actions related to this issue included enhancing torque specification values for the

packing, developing preventive maintenance items to re-torque the packing periodically,

and revising work packages. The inspectors determined these corrective actions were

reasonable and had been implemented appropriately and in a timely manner.

The inspectors also observed that appropriate effectiveness reviews were either

completed or were scheduled to be completed in a timely manner.

.4 Annual Sample: Human Performance Safety Culture Themes

a. Inspection Scope

This inspection focused on CENGs evaluation and resolution of an emerging theme in

the number of human performance cross-cutting issues associated with NRC inspection

findings. Specifically, in the third quarter of 2012, four NRC Green inspection findings

across multiple cornerstones were identified as having common cross-cutting aspects in

the area of Human Performance, Resources, H.2(c), because CENG did not provide

complete, accurate, and up-to-date procedures that were adequate to assure nuclear

safety. On August 9, 2012, CENG initiated CR-2012-007529 and performed an

apparent cause evaluation to assess this trend. The NRC completed Inspection

Procedure 71152 in the form of a problem identification and resolution annual sample to

assess this trend during the fourth quarter of 2012 to provide information to support the

end of cycle assessment. Subsequently, on November 7, CENG initiated CR-2012-

010211, A Cross-Cutting Theme Exists in the Aspect of Human Performance,

Resources, Documentation H.2(c), to further assess and address this adverse trend.

A root cause analysis was completed and corrective actions were recommended for

implementation. The inspectors selected this emerging trend for further review to

develop more recent insights into CENGs progress in addressing the cross-cutting

theme to provide meaningful input to the mid-cycle assessment process. The inspectors

reviewed CENG condition reports, the root cause evaluation, and corrective, preventive,

and compensatory actions associated with the emerging theme. The inspectors also

interviewed plant personnel. The four findings associated with cross-cutting theme

H.2(c) are summarized as follows:

Unit 1 - Inadequate torque applied to SDC isolation valve closure bolts (CR-2012-

001441)

Unit 2 - Loss of SFP cooling due an inadequate procedure (CR-2012-004850)

Unit 2 - Inadequate special operating procedure for loss of SFP cooling (CR-2012-

007811)

Unit 2 - Inadequate evaluation and implementation of design modification to the

turbine gland seal supply system (CR-2012-006615)

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b. Findings and Observations

No findings were identified.

CENG identified an adverse trend existed in the cross-cutting aspect H.2(c) and

recognized that the theme affected broad areas of performance as assessed in the

fourth quarter of 2012. CENG completed the root cause assessment for the adverse

trend in the H.2(c) cross-cutting aspect in December 2012. The root cause analysis

evaluated the four Green findings and also independently determined the common

causes of these findings.

CENG concluded that the work and administrative control documents and processes

were adequate, but the implementation of these processes was not adequate. Formal

techniques were used to reach this conclusion. The 46 specific causal factors from the

four findings were generalized into 13 general causal areas which were further

condensed (or binned) into five causal themes. The process of generalization of the

causal factors resulted in the majority of causal factors (53 percent) having the theme of

lack of engineering /challenge assumptions /mindset (willingness to accept answer with

no challenge). CENG further concluded a less rigorous standard resulted in products

that were of insufficient quality. The error drivers may be both process and behavior;

however, the results of the common cause analyses did not indicate that process

problems were significant errors.

CENG determined that the root cause of the trend was that site leadership had not

identified marginal performance relative to the technical rigor in the production of work

execution documents and, as such, has not put in place corresponding corrective or

mitigating strategies. A contributing cause was listed that existing administrative

controls governing changes to work orders and reviews of said changes are too lenient

to ensure high quality documents are consistently prepared to support plant operations

and maintenance activities.

The root cause team recommended 22 corrective actions in the report. CENG

management translated these recommendations into 20 unique corrective actions to be

implemented, 18 of which had been completed by the end of the first quarter 2013. The

two remaining corrective actions were to complete quarterly effectiveness reviews and a

final effectiveness review. The assigned corrective action to prevent recurrence

(CAPR159) was formulated to develop and communicate a station policy addressing

work documentation quality.

The corrective actions focused substantially on training plant personnel to properly

implement their procedures and to hold them accountable if they did not follow the

procedures. Three of the recommended corrective actions involved development of or

changes to work procedures. CA #59 was to define the term skill of the craft in a

procedure and was completed on June 12, using guidance obtained from an industry

group; CA #55 was to develop and implement a fleet conduct of engineering

administrative procedure and was closed to CA #244 to reinforce current expectations

for engineering roles and responsibilities; and CA #64 was to develop a process tool to

assist in screening pen and ink changes to procedures. This corrective action was also

changed to revise site procedures to add a requirement to initiate a condition report if a

procedure could not be completed as written. All but one corrective action relied on

knowledge-based corrective actions. The only rule-based corrective action was CA #59.

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Although the majority of the corrective actions were knowledge-based activities that

relied upon one-time training presentations, only two corrective actions were

implemented to conduct a needs analysis for the specified training. The needs analysis

for CA #58 (improve the use of SDS-006 for bolt-torque requirements) and CA #164

(understanding the work order process) both concluded that no additional or recurring

training were required. The one-time training that had been administered would be

sufficient to correct the adverse trend. As a result, no changes to the initial site training

program will be made and these training topics will not be refreshed periodically during

proficiency training.

The inspectors noted the implemented corrective actions rely almost entirely upon a

series of one-time training activities to result in institutionalized changes to personnel

behavior and organizational culture into the future. Therefore, the effectiveness of the

corrective actions could diminish over time as personnel turnover occurs.

The effectiveness reviews for the corrective actions are scheduled to start in the third

quarter of 2013. There have been no effectiveness reviews completed on the efficacy of

the corrective actions for this cross-cutting aspect theme as of June 2013.

The inspectors could not conclude that CENGs root cause analysis and resultant

corrective actions are correct and effective since they have only recently been fully

implemented. However, the number of findings with a cross-cutting aspect in procedure

adequacy has declined from four to two from the end of cycle to mid cycle NRC reviews.

.5 Annual Sample: Battery Low Specific Gravities

a. Inspection Scope

The inspectors performed an in-depth review of CENGs evaluations and corrective

actions associated with low-specific gravity in the safety-related station batteries.

Specifically, an adverse trend of low-specific gravity readings for cells in all three

safety-related 125 volts direct current (VDC) station batteries at Unit 2 were identified in

CR-2012-001315.

The inspectors assessed CENGs problem identification threshold, extent-of-condition

reviews, compensatory actions, and the prioritization and timeliness of CENGs

corrective actions to determine whether CENG was appropriately identifying,

characterizing, and correcting problems associated with this issue and whether the

planned and completed corrective actions were appropriate. The inspectors compared

the actions taken to the requirements of 10 CFR 50, Appendix B. In addition, the

inspectors performed field walkdowns and interviewed engineering personnel to assess

the effectiveness of the implemented corrective actions.

b. Findings and Observations

CENG determined the most probable cause of the low-specific gravities was that the

battery vendors had removed some electrolyte prior to shipping the battery cells to

NMPNS; and then once at NMPNS, water was added to the cells that diluted the

concentration of sulfuric acid.

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CENG performed a thorough review of the low-specific gravity issue and obtained

information from the battery vendors to support the probable cause. Corrective actions

included adjusting the method for calculating specific gravity and evaluating adding

electrolyte to restore the specific gravity to the manufacturers recommended level.

CENG verified, based on surveillance testing, that although the specific gravities were

lower than normal, the concentration of sulfuric acid was adequate to obtain sufficient

battery capacity to meet the design basis requirements of the batteries.

The inspectors reviewed condition reports, selected battery test results, and

correspondence from the battery vendors regarding the low-specific gravity issue. The

inspectors determined CENGs overall response to the issue was commensurate with

the safety significance, was timely and included appropriate compensatory actions. The

inspectors determined that the actions taken were reasonable to resolve the low-specific

gravity issue. As part of the review, the inspectors determined that two findings existed

as described below.

b.1 Inadequate Procedural Implementation for Battery Cell Replacement

Introduction. The inspectors identified a Green NCV of 10 CFR 50, Appendix B,

Criterion V, Instructions, Procedures, and Drawings, because CENG did not assure

that the replacement of cells in battery 2C was prescribed and performed by appropriate

procedures which resulted in degraded accuracy of test results and potential degradation

to safety-related battery cells.

Description. The Division III emergency battery bank, battery 2C, at Unit 2 uses jars that

contain three cells each to provide reliable direct current (DC) power for essential DC

loads required during normal and abnormal conditions. CENG determined that two jars

required replacing (a total of six cells). In preparation for this activity, CENG procured

three jars and stored them in the warehouse. The inspectors determined that several

procedural inadequacies existed during storage and subsequent cell replacement.

The cells in the warehouse were not monitored or maintained in accordance with vendor

recommendations. Specifically, the vendor requires that cells stored in spaces that are

not air conditioned should have individual cell voltages checked monthly and charged

when needed to prevent excessive discharge. Although CENG had previously noted

their poor practices with regards to battery storage and has ongoing corrective actions to

provide better storage facilities (as documented in CR-2010-012200), CENG did not take

action to adequately monitor cells in the warehouse. As a result, when the three jars for

battery 2C were obtained from the warehouse, one was found to be visibly sulfated and

had to be discarded, and the other two were found undercharged. Sulfation is an

indication of chronic undercharging and eventually results in permanent loss of capacity.

Although CR-2012-010907 identified the poor condition of the cells, the cell replacement

was continued with potentially degraded cells.

The newly installed cells were not charged prior to or upon installation. This is required

in the vendor manual and the station battery cell replacement procedure, N2-EMP-GEN-

673, 24/48 VDC and 125 VDC Batteries - Cell and Connector Replacement, Revision

00400.

Battery 2C was then subjected to a modified performance test with the newly installed

and uncharged cells. This resulted in over-discharging the new cells. Of the new cells,

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the two lowest reached 0.903 VDC and 1.167 VDC as opposed to the expected end

voltage of approximately 1.75 VDC. This resulted in a battery capacity of 95 percent. In

comparison a normal battery at the age of battery 2C would have a capacity of

approximately 105 percent. Using uncharged cells artificially lowered the test results

which diminished the ability to use the test results for future trending and could mask

poor performance of the remaining cells.

Finally, after the modified performance test, one of the new cells did not recharge

properly. Specifically the vendor states that an equalization charge should be performed

until the lowest cell is within 0.05 volt of the average of all of the cells. During the

equalization charge for battery 2C after the modified performance test, one of the new

cells did not rise to within 0.05 volt of the average of all of the cells. Although CR-2012-

010901 recognized that the acceptance criteria had not been met, the acceptance

criteria was determined to be unnecessary. CENG did not recognize that the failure to

recharge properly was an indication that the previous procedural inadequacies may have

degraded the cell.

CENG entered these inspector-identified issues into the CAP as CR-2013-005235.

CENG corrective actions included reviewing the previous battery 2C test results and the

work order for the next scheduled modified performance test and verifying battery 2C will

remain operable until the next test scheduled for September 2013. CENG also initiated

CR-2013-005074 to replace the two newly installed jars.

Analysis. The inspectors determined that the failure to assure that the replacement of

cells in battery 2C was prescribed and performed by appropriate procedures was a

performance deficiency that was reasonably within CENGs ability to foresee and correct

and should have been prevented. This finding was more than minor because it was

associated with the equipment performance attribute of the Mitigating Systems

cornerstone and affected the cornerstone objective of ensuring the availability, reliability,

and capability of systems that respond to initiating events to prevent undesirable

consequences.

In accordance with IMC 0609.04, Initial Characterization of Findings, and Exhibit 2 of

IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power,

issued June 19, 2012, the inspectors determined this finding to be of very low safety

significance (Green) because the performance deficiency was not a design or

qualification deficiency, did not involve an actual loss of safety function, did not represent

actual loss of a safety function of a single train for greater than its TS allowed outage

time, and did not screen as potentially risk significant due to a seismic, flooding, or

severe weather-initiating event.

This finding has a cross-cutting aspect in the area of Human Performance, Decision-

Making Component, because CENG did not use conservative assumptions in decision

making. Specifically, CENG did not monitor the cells in storage, question the adequacy

of the discharged cells, charge the cells prior to installation, or fully evaluate the

implications of the test and recharge results H.1(b).

Enforcement. 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and

Drawings, requires, in part, that activities affecting quality shall be prescribed by

documented instructions, procedures, or drawings of a type appropriate to the

circumstances and shall be accomplished in accordance with these instructions,

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procedures, or drawings. Contrary to the above, CENG did not assure that the

November 2012 replacement of cells in battery 2C was prescribed and performed by

appropriate procedures which resulted in degraded accuracy of test results and potential

degradation to safety-related battery cells. Because this violation was of very low safety

significance (Green) and has been entered into CENGs CAP (CR-2013-005235), this

violation is being treated as an NCV, consistent with Section 2.3.2 of the NRC

Enforcement Policy. (NCV 05000410/2013003-02, Inadequate Procedural

Implementation for Battery Cell Replacement)

b.2 Inadequate Design Control for Battery 2C

Introduction. The inspectors identified a Green NCV of 10 CFR Part 50, Appendix B,

Criterion III, Design Control, because CENG did not verify the adequacy of the design

with respect to battery 2C. Specifically, by failing to size the battery to the most limiting

time period, the sizing calculation significantly overstated the available design margin.

Description. The Division III emergency battery bank, battery 2C, uses jars that contain

three cells each to provide reliable DC power for essential DC loads required during

normal and abnormal conditions at Unit 2. The inspectors reviewed EC-145,

Verification of Adequacy of Division III Battery 2BYS*BAT2C, Revision 2, to determine

if the calculation appropriately verified the adequacy of the size of the installed battery

2C. The inspectors noted that the calculation evaluated the battery based on two time

periods, a 1-minute period and a 119-minute period. In accordance with Institute of

Electrical and Electronics Engineers (IEEE) Standard 485-1997, IEEE Recommended

Practice for Sizing Lead-Acid Batteries for Stationary Applications, and EC-145, the

battery should be sized based upon the most demanding time period. The inspectors

determined that the sizing was incorrect. Specifically, although EC-145 determined that

the first time period (1 minute) was the most demanding, the battery sizing was based

upon the less demanding second time period (119 minutes).

In response to this issue, CENG agreed that the calculation was incorrect, entered this

issue into their CAP (CR-2013-005117), and evaluated the condition for operability.

CENG performed the battery sizing calculation based upon the correct time period and

determined that the battery capacity margin reduced from 26 percent to negative

11 percent (i.e., the battery was undersized by 11 percent). CENG reduced the battery

design and aging margins from the calculation and were able to increase the capacity

margin to positive 10 percent which demonstrated a reasonable expectation of

operability. The significance of reducing the design margin was that the original

calculation would have permitted modifications to the Division III DC system that could

have actually overloaded the battery. The significance of reducing the aging margin is

that the battery would not have been able to perform its design function as the battery

aged.

The inspectors independently performed battery sizing calculations and agreed with

CENGs results.

Analysis. The inspectors determined that the failure to verify the adequacy of the design

with respect to battery 2C was a performance deficiency that was reasonably within

CENGs ability to foresee and correct and should have been prevented. This finding was

more than minor because it was associated with the design control attribute of the

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Mitigating Systems cornerstone and affected the cornerstone objective of ensuring the

availability, reliability, and capability of systems that respond to initiating events to

prevent undesirable consequences.

In accordance with IMC 0609.04, Initial Characterization of Findings, and Exhibit 2 of

IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power,

issued June 19, 2012, the inspectors determined this finding is of very low safety

significance (Green) because the performance deficiency was not a design or

qualification deficiency, did not involve an actual loss of safety function, did not represent

actual loss of a safety function of a single train for greater than its TS allowed outage

time, and did not screen as potentially risk-significant due to a seismic, flooding, or

severe weather-initiating event.

This finding did not have a cross-cutting aspect because it was not indicative of current

performance. Specifically, EC-145 was last revised in 2008.

Enforcement. 10 CFR 50, Appendix B, Criterion III, Design Control, states, in part, that

design control measures shall provide for verifying or checking the adequacy of design.

Contrary to the above, from July 17, 2008, to June 12, 2013, CENGs design control

measures had not appropriately verified the adequacy of the design regarding battery

2C. Specifically, by failing to size the battery to the most limiting time period, the sizing

calculation significantly overstated the available design margin. Because this violation

was of very low safety significance (Green) and has been entered into CENGs CAP

(CR-2013-005117), this violation is being treated as an NCV, consistent with Section

2.3.2 of the NRC Enforcement Policy. (NCV 05000410/2013003-03, Inadequate

Design Control for Battery Sizing Calculation)

4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153 - 6 samples)

.1 Plant Events

a. Inspection Scope

For the plant events listed below, the inspectors reviewed and/or observed plant

parameters, reviewed personnel performance, and evaluated performance of mitigating

systems. The inspectors communicated the plant events to appropriate regional

personnel, and compared the event details with criteria contained in IMC 0309,

Reactive Inspection Decision Basis for Reactors, for consideration of potential reactive

inspection activities. As applicable, the inspectors verified that CENG made appropriate

emergency classification assessments and properly reported the event in accordance

with 10 CFR Parts 50.72 and 50.73. The inspectors reviewed CENGs follow-up actions

related to the events to assure that CENG implemented appropriate corrective actions

commensurate with their safety significance.

Unit 1 loss of battery board 12 and SDC on April 16, 2013

Loss of all SDC pumps for 17 minutes on April 16, 2013

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b. Findings

Introduction. The inspectors documented an apparent violation of Unit 1 TS 6.4.1,

Procedures, because CENG failed to properly restore from a loss of a vital DC bus in

accordance with station off-normal procedures resulting in an unplanned loss of all SDC

when time to boil was less than 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />. Specifically, operators failed to recognize a

potential for loss of SDC during battery bus 12 restoration in accordance with N1-SOP-

47A.1, Loss of DC, Revision 00101, and N1-OP-47A, VDC Power System, Revision

02500.

Description. Unit 1 shut down for a refueling outage on April 15, 2013. On April 16,

Unit 1 was in cold shutdown at 118 degrees Fahrenheit with a temperature band of 110

to 120 degrees Fahrenheit. The reactor vessel head was installed, and the head bolts

were in the process of being detensioned in preparation for reactor cavity flood up and

reactor vessel head removal. Primary containment was open for planned maintenance.

Decay heat removal was via the SDC pump 12. SDC pumps 11 and 13 were secured

with their breakers racked out to the test position for planned loss of offsite power/loss of

coolant accident testing (LOOP/LOCA).

During LOOP/LOCA testing, the SDC pumps and ECCS pumps in train associated with

the bus are racked to their test position. Operators are stationed in the field to restore

these pumps to normal so the pumps are still considered to be available. This is

permitted by NMPNS TSs; however, automatic functions of the pumps are not available

(such as auto start on a low-low reactor vessel level signal).

At 2:45 p.m. on April 16, a contractor walking down a tagout associated with an ERV

modification made an error and opened the breaker cabinet door for the vital DC bus 12.

The vital DC bus 12 cabinet door contains a mechanical interlock which opens battery

breaker 12 and the static battery charger DC output breaker, de-energizing the DC

switchgear when the door is open. Upon opening the breaker cabinet door and hearing

the breakers trip, the contractor realized he was in the incorrect cabinet and immediately

contacted the control room and notified them of the event. The vital bus was considered

protective equipment and a sign on the cabinet door cautioned that the door interlock

would trip the breakers in that cabinet. The loss of the vital DC bus 12 resulted in a

partial loss of indication in the main control room, loss of DC control power for the

associated bus, and a high-temperature trip signal for the SDC 12 being generated.

However, since DC power to the trip solenoid was also lost, the SDC pump 12 continued

to run. The ECCS pumps associated with the #12 bus were inoperable due to loss of

control power.

In response to the event, operators entered procedure N1-SOP-47A, Loss of DC,

Revision 00101. The flowchart in SOP-47A.1 directs the operator to transfer selected

loads normally powered from battery bus 12 to their alternate power supplies and then

directs restoration of the bus. However, a decision was made to not take actions

specified in N1-SOP-47A.1 and pursue restoring the vital DC bus 12 using system

operating procedure N1-OP-47A, 125 VDC Power System, Revision 02500. The

inspectors noted that N1-SOP-47A.1 Section 5.1 contains two caution statements stating

that pump trip signals may have been generated while the bus was de-energized and

those signals must be cleared prior to restoration or a pump trip may occur when the bus

is restored and power is supplied to the DC trip coils. However, neither N1-SOP-47A.1

nor N1-OP-47A contained a list of tripping circuits and tripping actions which are

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associated with the vital DC bus 12. Operators failed to recognize the bus 12

high-temperature trip signal present on the alarm log and the plant process computer

displays prior to attempting to restore bus 12. The presence of the trip signal was also

indicated by a control room annunciator which was locked-in since the loss of battery

bus 12 at 2:45 p.m.

At 3:45 p.m., field operators attempted to close static battery charger 171A DC output

breaker to restore the battery bus from its alternate power supply. Due to the high-

temperature trip signal already being present on the SDC pump 12, when operators

attempted to close the static battery charger 171A output breaker, the DC trip coil

received enough power to energize the relay and trip the SDC pump 12 just before the

static battery charger 171A output breaker tripped due to the mechanical interlock.

Operators did not immediately recognize that they had lost SDC pump 12 via their

indications at the control panel (i.e.; annunciator, pump current, pump flow). Upon

recognizing the loss of SDC at approximately 3:50 p.m., operators entered N1-SOP-6.1

Loss of SFP/RX Cavity Level/Decay Heat Removal, Revision 00501.

At 3:50 p.m., the control room directed the breakers for SDC pumps 11 and 13 to be

racked to their normal positions and that SDC be restored using the 11 and 13 SDC

pumps. The 11 SDC pump breaker was restored at 4:03 pm and SDC flow was restored

at 4:17 pm when the SDC 11 temperature control valve was opened, restoring cooling

flow to the reactor. Reactor vessel temperature rose from 118 to 145 degrees

Fahrenheit as a result of the loss of SDC. At 5:11 p.m., the normal DC power

distribution lineup was restored.

CENG immediately conducted prompt investigations of both the loss of battery bus 12

and loss of SDC events, entered both events into their CAP as CR-2013-002926 and

CR-2013-002916, and conducted a root cause analysis. CENG determined the root

cause for the loss of SDC was inadequate procedural guidance for restoring the DC

power. Contributing causes included operators proceeding in the face of uncertainty,

management oversight of operations, and inadequate use of operational experience

which could have precluded this event. Corrective actions to prevent recurrence

included a review of operations procedures to ensure those procedures contain

adequate levels of detail to safely recover from the event and restore the system to

normal operation.

Analysis. The inspectors determined that CENGs failure to properly restore the battery

bus 12 in accordance with plant procedures was a performance deficiency that was

reasonably within CENGs ability to foresee and correct and should have been

prevented. The performance deficiency was determined to be more than minor because

the inspectors determined it affected the configuration control aspect of the Initiating

Events cornerstone and adversely affected the associated cornerstone objective to limit

the likelihood of events that upset plant stability and challenge critical safety functions

during shutdown as well as power operations. Specifically, operators failed to recognize

a potential for loss of SDC during battery bus 12 restoration in accordance with N1-SOP-

47A.1, Loss of DC, Revision 00101, and N1-OP-47A, VDC Power System, Revision

02500. This performance deficiency initiated a plant transient, loss of shutdown cooling.

The inspectors evaluated the finding using IMC 0609 Attachment 0609.04, Initial

Characterization of Findings, issued June 19, 2012, and IMC 0609 Appendix G,

Shutdown Operations Significance Determination Process, issued February 28, 2005.

Enclosure

45

IMC 0609 Appendix G Table 1, Losses of Control, states a quantitative analysis is

required for:

Loss of Thermal Margin (PWRs and BWRs)

(Inadvertent change in RCS temperature due to loss of RHR)/(change in temperature

that would cause boiling) > 0.2 (temperature margin to boil)

In this case, RCS temperature changed 27 degrees (145 to 118 degrees Fahrenheit)

and the change in temperature to boiling was 94 degrees (212 to 118 degrees

Fahrenheit). Temperature margin to boil was greater than 0.2 (0.2872); thus, a

quantitative analysis was required. The significance of the finding is designated as To

Be Determined (TBD) until a Phase 3 analysis can be completed by Regional and

Headquarters Senior Reactor Analysts.

The inspectors determined this finding had a cross-cutting aspect in the area of Human

Performance, Resources, because CENG did not ensure that personnel, equipment,

procedures, and other resources were available and adequate to assure nuclear safety -

complete, accurate and up-to-date design documentation, procedures, and work

packages, and correct labeling of components. Specifically, CENG procedures

N1-SOP-47A.1 and N1-OP-47A did not contain adequate guidance to ensure recovery

from a loss of a DC bus would not result in an unexpected plant transient H.2(c).

Enforcement. Unit 1 TS 6.4.1, Procedures, requires, in part, that written procedures

and administrative policies shall be established, implemented, and maintained that meet

or exceed the requirements and recommendations of Sections 5.1 and 5.3 of American

National Standards Institute N18.7-1972 Administrative Controls and Quality Assurance

for the Operational Phase of Nuclear Power Plants, and cover the following activities:

the applicable procedures recommended in RG 1.33, Quality Assurance Program

Requirements (Operation), Appendix A, Typical Procedures for Pressurized-Water

Reactors and Boiling-Water Reactors, dated November 3, 1972. RG 1.33, Appendix A,

Section 4, Procedure for Startup, Operation, and Shutdown of Safety-Related BWR

Systems, requires procedures for onsite DC system, and Section 6, Procedures for

Combating Emergencies and Other Significant Events, requires, in part, procedures for

including loss of electrical power (and/or degraded power sources). CENG procedures

N1-OP-47A, 125 VDC Power System, Revision 02500, and N1-SOP-47A.1, Loss of

DC, Revision 00101, implement this requirement. Contrary to the above, on April 16,

2013, operators were unable to properly implement N1-OP-47 and N1-SOP-47A.1

following a loss of the battery bus 12 resulting in a temporary loss of all decay heat

removal. This issue is being characterized as an apparent violation in accordance with

the NRC's Enforcement Policy, and its final significance will be dispositioned in a

separate future correspondence. (Apparent Violation 05000220/2013003-04,

Improper Bus Restoration Results in a Loss of Shutdown Cooling)

.2 (Closed) LER 05000220/2012-006-00: Technical Specification Required Shutdown Due

to Containment Leakage

a. Inspection Scope

On December 13, 2012, Unit 1 commenced a shutdown after observing nitrogen leakage

from primary containment over a period of 10 days. NRC Inspection Report

Enclosure

46

05000220/2012005 documented CENGs immediate response and the NRCs initial

review of the event. As of the end of the inspection documented in that report, CENGs

evaluation of the causes for the leakage was still ongoing. The inspectors had identified

an issue of concern regarding the total amount of leakage from primary containment

vent and purge valves and its relation to exceeding the required value in TS 3.3.3. The

NRC opened URI 05000220/2012005-03 to track CENGs completion of the root cause

evaluation, the quantification of the amount of leakage from primary containment for the

event, and the NRCs subsequent review of CENGs completed evaluation.

To close URI 05000220/2012005-03 the inspectors reviewed and independently verified

CENGs calculation regarding the quantity of leakage from primary containment from

December 3 - December 13. The inspectors also reviewed Appendix J Type B and C

testing of the primary containment vent and purge valves to determine leakage

quantities and how they impacted overall primary containment leakage. The inspectors

also reviewed the cause of the leakage and CENGs actions to address the cause which

was included in CR-2012-011157. URI 05000220/2012005-03 is closed to the violation

discussed below. The enforcement actions associated with this LER are discussed

below. This LER is closed.

b. Findings

Introduction. A self-revealing Green NCV of TS 3.3.3, Leakage Rate, was identified for

CENGs failure from December 3 to December 13, 2012, to maintain containment

leakage less than 1.5 percent by weight of the containment air per day and less than 0.6

percent by weight of the containment air per day for all penetrations and all primary

containment isolation valves subject to 10 CFR Part 50, Appendix J, Types B and C

tests, when pressurized to 35 pounds per square inch gauge (psig) when RCS

temperature is above 215 degrees Fahrenheit and primary containment integrity is

required.

Description. On December 3, 2012, at 11:31 a.m., Unit 1 established primary

containment integrity and commenced a reactor startup from an unplanned outage. The

following day at 2:40 a.m., CENG operators commenced adding nitrogen gas into the

primary containment as part of a planned activity to reduce primary containment oxygen

concentration to less than 4 percent as required by TS 3.3.1, Oxygen Concentration.

This activity was completed at 10:55 a.m. on December 4. Once an appropriate nitrogen

concentration has been achieved in the containment, additional makeup is generally not

required. However, from December 6 through December 8, on three occasions,

operators added additional nitrogen to the containment to maintain pressure within

procedural limits. This issue was documented in CR-2012-011157, Adverse Trend in

Unit 1 Nitrogen Usage. CENG commenced initial troubleshooting activities which

included examining systems and components that were possible sources of nitrogen

leakage; however, a definitive source for the leakage was not identified. On

December 12, following a fourth addition of nitrogen, CENG increased the importance of

the issue, formed an issue response team, and staffed the outage control center. As

part of the investigation process, operators cycled several containment isolation valves

in the nitrogen purge and vent system and attempted to quantify the amount of seat

leakage through the valves by opening test fittings located between isolation valves. In

parallel with the troubleshooting efforts, CENG and vendor personnel began to develop

analytical tools that could be used to quantify the amount of containment leakage.

Enclosure

47

On December 13, at 6:47 p.m., after observing a decrease in containment pressure

following a fifth nitrogen addition and receiving preliminary data that a containment

isolation valve local leak-rate test between reactor containment inert gas purge and fill

drywell cooling system isolation valves IV-201-31 and IV-201-32 may fail, CENG

commenced a plant shutdown because primary containment integrity as required in TS 3.3.3 could not be assured. On December 13, at 11:33 p.m., the plant reached cold

shutdown and exited plant TS 3.3.3.

Subsequent testing of containment isolation valves revealed that three valves in the

reactor containment inert gas purge and fill drywell cooling system, valves IV-201-10,

IV-201-31, and IV-201-32 had unacceptable seat leak rates. These conditions were

documented in condition reports 2012-011210 and 2012-011288. When the valves were

disassembled and examined, CENG identified that iron oxide (i.e., rust) buildup on the

valve resilient seats had prevented the valves from closing tightly and adversely

impacted seat leakage performance. The reactor containment inert gas purge and fill

drywell cooling system is a carbon steel system and the internal piping surface adjacent

to the valves had visible signs of iron oxide degradation. CENG corrective actions

included removing the loose surface rust, installing new resilient seats on the valves,

and successfully performing as-left local leak-rate tests on the subject valves. Additional

corrective actions were outlined in CR-2012-011247.

CENG analysis determined that based upon the nitrogen supplied to the drywell,

containment leakage from December 3 through December 13, 2012, exceeded the limits

in TS 3.3.3 which requires containment leakage to be less than 1.5 percent by weight of

the containment air per day and less than 0.6 percent by weight of containment air per

day for all penetrations and all primary containment isolation valves subject to 10 CFR Part 50, Appendix J, Types B and C tests, when pressurized to 35 psig when RCS

temperature is above 215°F and primary containment integrity is required. Specifically,

leakage was calculated to be between 1,421 and 2,023 standard cubic feet per hour

verses a calculated limit of 647 standard cubic feet per hour.

Analysis. The inspectors determined that CENGs failure to maintain containment

leakage from December 3 through December 13, 2012, within the limits required by TS 3.3.3 was a performance deficiency that was within CENGs ability to foresee and

correct and should have been prevented. This finding is more than minor because it is

associated with the SSC and barrier performance attribute of the Barrier Integrity

cornerstone and affected the cornerstone objective to provide reasonable assurance that

physical design barriers (fuel cladding, RCS, and containment) to protect the public from

radionuclide releases caused by accidents or events. Specifically, containment leakage

from December 3 through December 13 exceeded the leakage limits outlined in Unit 1

TS 3.3.3.

In accordance with IMC 0609.04, Initial Characterization of Findings, and Table 6.2,

Phase 2 Risk Significance-Type B Findings at Full Power, of IMC 0609, Appendix H,

Containment Integrity Significance Determination Process, issued May 6, 2004, the

inspectors determined this finding was of very low safety significance (Green) because

the leakage was less than 100 percent of containment volume per day for the duration of

the leak.

This finding has a cross-cutting aspect in the area of Problem Identification and

Resolution, CAP, because CENG failed to take appropriate corrective action to address

Enclosure

48

safety issues and adverse trends in a timely manner commensurate with their safety

significance. Specifically, following identification of the adverse trend regarding the

frequency of nitrogen addition to the drywell, CENG did not assess in a timely manner

the significance of the leakage and the impact on primary plant containment. As a

result, plant operation continued for several days with drywell leakage that exceeded the

limits outlined in TS 3.3.3 P.1(d).

Enforcement. TS 3.3.3, Leakage Rate, requires containment leakage to be less than

1.5 percent by weight of the containment air per day and less than 0.6 percent by weight

of the containment air per day for all penetrations and all primary containment isolation

valves subject to 10 CFR Part 50, Appendix J, Types B and C tests, when pressurized

to 35 psig when RCS temperature is above 215 degrees Fahrenheit and primary

containment integrity is required. Contrary to the above, from December 3 through 13,

2012, containment leakage exceeded 1.5 percent by weight. Specifically, following a

December 13 plant shutdown, CENG determined containment leakage during this period

to have been between 1,421 and 2,023 standard cubic feet per hour verses a calculated

limit of 647. Because this violation is of very low safety significance (Green) and CENG

entered this issue into their CAP as CR-2013-011247, this finding is being treated as an

NCV consistent with consistent with Section 2.3.2 of the NRC Enforcement Policy.

(NCV 05000220/2013003-05, Containment Leakage Exceeds Technical

Specification 3.3.3 Limits)

.3 (Closed) LER 05000220/2012-006-01: Technical Specification Required Shutdown Due

to Containment Leakage

This LER was revised on June 14, 2013, to reflect changes in corrective actions that

were outlined in the original LER submittal. In the original LER, CENG indicated that

during the spring 2013 refueling outage, the internal surfaces of the horizontal drywell

vent and purge piping that contained valves IV-201-09, IV-201-10, IV-201-31, and

IV-201-32 would be coated with a material that would minimize the recurrence of rust

buildup on the piping. Further, during the outage, the vertical piping that contained

valves IV-201-07, IV-201-08, IV-201-16, and IV-201-17 would be inspected; and based

on the inspection findings, a coating strategy (if required) would be developed for that

piping. Subsequent to submittal of the original LER, CENG determined that based upon

the difficultly associated with application of a suitable coating to the pipes and the

potential of subsequent coating failure, a protective coating would not be installed.

In lieu of the original corrective actions, CENG indicated that the horizontal section of

pipe would be inspected each refueling outage. The vertical piping would not be

inspected. These corrective actions were based, in part, on results from inspections

conducted during the 2013 N1R22 that identified rust accumulation only on the

horizontal sections of pipe. The enforcement aspects of this issue are discussed in

section 4OA3.2 of this report. The inspectors did not identify any new issues during the

review of this revised LER. This LER is closed.

.4 (Closed) LER 05000220/2012-007-00: High-Pressure Coolant Injection System Logic

Actuation Following an Automatic Turbine Trip Signal due to High Reactor Water Level

On November 6, 2012, while Unit 1 was in cold shutdown, an unexpected rise in reactor

water level occurred causing an automatic turbine trip signal and actuation of the

high-pressure coolant injection initiation logic. Operators immediately closed the 12

Enclosure

49

feedwater pump discharge blocking valve and stabilized reactor water level, stopping the

transient. At Unit 1, high-pressure coolant injection is a mode of operation of the

condensate and feedwater system that utilizes the condensate storage tanks, main

condenser hotwell, two condensate pumps, two feedwater booster pumps, and two

motor-driven feedwater pumps. The rise in reactor water level resulted from the 12

feedwater flow control valve (FCV) FCV-29-137 unexpectedly failing partially open when

instrument air was removed from the valve during a tagout in preparation for

maintenance on the valve. FCV-29-137 has a series of lockup valves that are designed

to hold the FCV stem in position in the event instrument air is lost. CENG determined

FCV-29-137 partially opened due to a degraded top cylinder lockup valve O-ring. The

enforcement aspects of this issue are discussed in NRC Integrated Inspection Report 05000220/2013002, Section 1R22. The inspectors did not identify any new issues

during the review of the LER. This LER is closed.

.5 (Closed) LER 05000410/2013-001-00: Reactor Core Isolation Cooling System Isolation

Due to a Temperature Switch Unit Failure

On January 23, 2013, at 3:16 p.m., Unit 2 was operating at 100 percent power when an

unexpected isolation signal for containment isolation valves in the RCIC and RHR

system occurred due to a failure of a RB general area temperature switch

(2RHS*TS85A). The isolation resulted in the RCIC system being unavailable for

injection into the reactor vessel if called upon during an event. The affected RHR

isolation valves were already in the closed position which is their normal position during

power operation. The failure also occurred concurrently with the HPCS system being

inoperable for planned surveillance testing. With both RCIC and HPCS inoperable,

high-pressure coolant makeup capability was lost. At 3:50 p.m., HPCS was restored

and declared operable. Temperature switch 2RHS*TS85A was replaced at 11:04 p.m.,

and on January 24, at 1:17 a.m., RCIC was declared operable. The cause of the

temperature switch failure was determined to be age-related capacitor degradation. The

enforcement aspects of this issue are discussed in NRC Integrated Inspection Report 05000410/2013002, Section 1R12. The inspectors did not identify any new issues

during the review of the LER. This LER is closed.

.6 (Closed) LER 05000410/2013-002-00: Failure of High-Pressure Core Spray System

Pressure Pump Due to Motor Winding Failure

On February 28, 2013, Unit 2 was operating at 100 percent power when the HPCS

system pressure pump failed. At the time of the failure, the HPCS system was

inoperable for planned maintenance. The pump failure was due to turn-to-turn short in

the motor winding. The HPCS system pressure pump is designed to maintain a positive

pressure on the HPCS discharge header to prevent voids from forming. CENG replaced

the HPCS pressure pump motor and returned the HPCS system to an operable status

on March 6. The HPCS system discharge piping remained full during the period when

the pressure pump was OOS. The inspectors reviewed the maintenance history of the

HPCS pressure pump motor and determined that when the motor bearings were

replaced in January 2011, the work order documented a satisfactory visual inspection

and meggar testing of the motor windings. The inspectors reviewed the LER and

determined that no findings or violations of NRC requirements were identified. This LER

is closed.

Enclosure

50

4OA6 Meetings, Including Exit

Exit Meeting

On July 25, 2013, the inspectors presented the inspection results to Mr. Christopher

Costanzo, Site Vice President, and other members of the NMPNS staff. The inspectors

verified that no propriety information was retained by the inspectors or documented in

this report.

ATTACHMENT: SUPPLEMENTARY INFORMATION

Enclosure

A-1

SUPPLEMENTARY INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

C. Costanzo, Vice President

J. Stanley, Plant General Manager

P. Bartolini, Supervisor, Design Engineering

K. Clark, Director, Security

S. Dack, Seasonal Readiness Coordinator / Cycle Manager

J. Dean, Supervisor, Quality Assurance

S. Dhar, Design Engineering

J. Dosa, Director, Licensing

J. Gillard, Emergency Preparedness Analyst

J. Holton, Supervisor, Systems Engineering

G. Inch, Principle Engineer,

M. Kunzwiler, Security Supervisor

J. Leonard, Supervisor Design Engineering

C. McClay, Senior Engineer

F. Payne, Manager, Operations

P. Politzi, Work Week Manager

J. Reid, Design Engineer

B. Scaglione, System Engineer

J. Schulz, System Engineer

M. Shanbhag, Licensing Engineer

R. Staley, System Engineer

T. Syrell, Manager, Nuclear Safety and Security

J. Thompson, General Supervisor, Mechanical Maintenance

A. Verno, Director, Emergency Preparedness

Attachment

A-2

LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED

Opened

05000220/2013003-04 AV Improper Bus Restoration Results in a Loss of

Shutdown Cooling (Section 4OA3)

Opened/Closed

05000410/2013003-01 NCV Failure to Follow Containment Isolation System

Surveillance Procedure Resulting in Isolation of the

Reactor Coolant Isolation Cooling System

(Section 1R22)05000410/2013003-02 NCV Inadequate Procedural Implementation for Battery

Cell Replacement (Section 4OA2)05000410/2013003-03 NCV Inadequate Design Control for Battery Sizing

Calculation (Section 4OA2)05000220/2013003-05 NCV Containment Leakage Exceeds Technical

Specification 3.3.3 Limits (Section 4OA3)

Closed

05000220/2012005-03 URI Assessment of Containment Leakage Due to

Containment Isolation Valve Failure (4OA3)

05000220/2012-006-00 and LER Technical Specification Required Shutdown Due

05000220/2012-006-01 to Containment Leakage (Section 4OA3)

05000220/2012-007-00 LER High-Pressure Coolant Injection System Logic

Actuation Following an Automatic Turbine Trip

Signal Due to High Reactor Water Level

(Section 4OA3)

05000410/2013-001-00 LER Reactor Core Isolation Cooling System Isolation

Due to a Temperature Switch Unit Failure

(Section 4OA3)

05000410/2013-002-00 LER Failure of High-Pressure Core Spray System

Pressure Pump Due to Motor Winding Failure

(Section 4OA3)

Attachment

A-3

LIST OF DOCUMENTS REVIEWED

Section 1R01: Adverse Weather Protection

Procedures

N1-OP-64, Meteorological Monitoring, Revision 00603

N2-OP-102, Meteorological Monitoring, Revision 01103

N2-OP-102, Attachment 3, Hot Weather Preparation Checklist, Revision 01102

NAI-PSH-11, Seasonal Readiness Program, Revision 00700

Condition Reports

CR-2010-008430 CR-2011-010519 CR-2012-004448

CR-2011-008564 CR-2012-001034 CR-2012-007341

CR-2011-009058 CR-2012-002008 CR-2013-000154

CR-2011-009946 CR-2012-004258

Work Orders

WO C90679919 WO C91901545 WO C92110489

WO C91178423 WO C91919260 WO C92116209

WO C91425002 WO C91920244 WO C92133487

WO C91570604 WO C91966877 WO C92135500

WO C91570606 WO C92033133 WO C92139868

WO C91711577 WO C92008152 WO C92154168

WO C91847825 WO C92008169 WO C92156668

WO C91860534 WO C92015166 WO C92156894

WO C91862547 WO C92044771 WO C92161257

WO C91862559 WO C92067054 WO C92221738

WO C91883258 WO C92073630 WO C92226912

WO C91883511 WO C92073671 WO C92285675

WO C91883613 WO C92073704 WO C92292596

WO C91897710 WO C92107827

Miscellaneous

Diesel Trend Analysis

Summer Readiness Status, Attachment 1

System Seasonal Readiness Evaluations, Attachment 2

Unit 1 Scheduler Evaluation for Summer Readiness from June 15 to September 15

Unit 2 Scheduler Evaluation for Summer Readiness from June 15 to September 15

Section 1R04: Equipment Alignment

Procedures

N1-OP-13, Emergency Cooling System, Revision 03700

N1-OP-48, Control Room Ventilation System, Revision 02400

NIP-OUT-01, Shutdown Safety, Revision 03700

Attachment

A-4

Condition Reports

CR-2013-004333

CR-2013-004347

Drawings

B-69017-C, Emergency Condenser Number 11 Steam Flow, Revision 1

C-180007-C, Reactor Core Spray Piping and Instrumentation Drawing (P&ID), Revision 58

C-18008-C, Spent Fuel Storage Pool Filtering and Cooling System, Revision 38

C-18030-C, Fire Protection Water System, Revision 38

C-18047-C, Control Room Heating Ventilation and Air Conditioning System, Revision 48

C-181017-C, Emergency Cooling System, Revision, Revision 55

Miscellaneous

Plant Configuration Change 1M00888

Section 1R05: Fire Protection

Procedure

N1-PFP-0101, Unit 1 Pre-Fire Plans, Revision 00200

Condition Report

CR-2013-002902

Miscellaneous

USAR Section 10, Revision 16

Section 1R07: Heat Sink Performance

Procedure

N1-ST-Q25, Emergency Diesel Generator Cooling Water Quarterly Test, Revision 02201

Work Order

WO C91454468

Section 1R08: In-Service Inspection

Procedures

NDEP-PT-3.00, Liquid Penetrant Examination, Revision 01900

NDEP-UT-6.23, UT Examination of Ferritic Piping Welds, Revision 01100

NDEP-UT-6.24, UT Examination of Austenitic Piping Welds, Revision 01101

NDEP-VT-2.01, ASME Section XI Visual Examination, Revision 19

NDEP-VT-2.07, In-Vessel Visual Examination, Revision 1300

NIP-IIT-02, ASME Section XI Repair and Replacement Program, Revision 00701

SI-UT-130, Phased Array Ultrasonic Examination of Dissimilar Metal Welds, Revision 0

Condition Reports

CR-2012-000816

Attachment

A-5

CR-2012-003805

CR-2012-010291

CR-2013-000506

CR-2013-001573

CR-2013-002975

CR-2013-002977

CR-2013-002978

CR-2013-003442

Drawing

C-18009, Reactor Water Cleanup P&ID, Revision 60, Sheet 1

Work Order

WO C92260831

NDE Records

BOP-UT-13-014, UT Calibration/Thickness Examination Records of RBCLC System Piping to

Recirculation Pump 11 Motor MOT-32-187, dated April 21, 2013

BOP-UT-13-015, UT Calibration/Thickness Examination Records of RBCLC System Piping to

Recirculation Pump 12 Motor MOT-32-188, dated April 21, 2013

BOP-UT-13-016, UT Calibration/Thickness Examination Records of RBCLC System Piping to

Recirculation Pump 13 Motor MOT-32-189, dated April 21, 2013

BOP-UT-13-017, UT Calibration/Thickness Examination Records of RBCLC System Piping to

Recirculation Pump 14 Motor MOT-32-190, dated April 21, 2013

BOP-UT-13-018, UT Calibration/Thickness Examination Records of RBCLC System Piping to

Recirculation Pump 15 Motor MOT-32-191, dated April 21, 2013

BOP-UT-13-021, UT Calibration/Thickness Examination Records of General Corrosion of

RBCLC System Piping Inside U1 Drywell 225 Feet Elevation, dated April 24, 2013

ISI-PT-13-003, Liquid Penetrant Examination Record of Branch Connection - Decontamination

Port Weld 32-WD-011 on Recirculation System Suction Piping, dated April 24, 2013

ISI-PT-13-004, Liquid Penetrant Examination Record of Branch Connection - Decontamination

Port Weld 32-WD-091 on Recirculation System Suction Piping, dated April 24, 2013

ISI-UT-13-032, UT Calibration/Examination Records of Branch Connection - Decontamination

Port Weld 32-WD-051 on Recirculation System Suction Piping, dated April 22, 2013

ISI-UT-13-033, UT Calibration/Examination Records of 12-Inch Diameter Emergency Condenser

Supply Piping, Pipe-to-Pipe Weld 39-WD-108, dated April 24, 2013

ISI-UT-13-034, UT Calibration/Examination Records of 12-Inch Diameter Emergency Condenser

Supply Piping, Pipe-to-Tee Weld 39-WD-109, dated April 24, 2013

ISI-UT-13-035, UT Calibration/Examination records of 12-Inch Diameter Emergency Condenser

Supply Piping, Tee-to-Pipe Weld 39-WD-110, dated April 24, 2013

ISI-UT-13-036, UT Calibration/Examination Records of 12-Inch Diameter Emergency Condenser

Supply Piping, Pipe-to-Elbow Weld 39-WD-112, dated April 20, 2013

NMP U1 33-WD-046, Phased Array UT Calibration/Examination Records of 6-Inch Diameter

RBCLC Pipe-to-Pipe DM Weld, dated April 29, 2013

UT Calibration/Examination Records of Unit 1 32-WD-042, N2A Safe End-Nozzle DM Weld,

Phased Array Ultrasonic Examination Record, dated April 30, 2013

UT Calibration/Examination Records of Unit 1 32-WD-042, N2A Safe End-to-Nozzle DM Weld

on Recirc Discharge, Phased Array Ultrasonic Examination Record, dated April 30, 2013

UT Calibration/Examination Records of Unit 1 32-WD-082, N2B Safe End-to-Nozzle DM Weld

on Recirc Discharge, Phased Array Ultrasonic Examination Record, dated April 30, 2013

Attachment

A-6

UT Calibration/Examination Records of Uni5 1 32-WD-122, N2C Safe End-to-Nozzle DM Weld

on Recirc Discharge, Phased Array Ultrasonic Examination Record, dated April 30, 2013

UT Calibration/Examination Records of Unit 1 32-WD-164, N2D Safe End-to-Nozzle DM Weld

on Recirc Discharge, Phased Array Ultrasonic Examination Record, dated April 30, 2013

UT Calibration/Examination Records of Unit 1 32-WD-208, N2E Safe End-to-Nozzle DM Weld

on Recirc Discharge, Phased Array Ultrasonic Examination Record, dated April 30, 2013

Miscellaneous

Audit Report SPC-12-01-N, Special Processes, Testing, & Inspection, dated November 28, 2012

ASME, 2004 Edition

Section 1R11: Licensed Operator Requalification Program and Licensed Operator

Performance

Procedure

CNG-OP-1.01-1000, Conduct of Operations, Revision 00900

Condition Reports

CR-2013-002697

CR-2013-002698

CR-2013-002647

CR-2013-002652

Section 1R12: Maintenance Effectiveness

Procedures

CNG-AM-1.01-1023, Maintenance Rule Program, Revision 00201

N2-OP-33, High Pressure Core Spray System, Revision 01201

N2-OSP-CSH-Q@002, HPCS Pump and Valve Operability and System Integrity Test,

Revision 00500

Condition Reports

CR-2011-006564 CR-2012-002176 CR-2012-009400

CR-2011-006930 CR-2012-002198 CR-2012-009982

CR-2011-007084 CR-2012-002249 CR-2012-010499

CR-2011-007313 CR-2012-002711 CR-2013-000159

CR-2011-007654 CR-2012-005017 CR-2013-000563

CR-2011-007830 CR-2012-005119 CR-2013-001491

CR-2011-009790 CR-2012-005999 CR-2013-001633

CR-2011-010817 CR-2012-006141 CR-2013-002768

CR-2012-000359 CR-2012-007193 CR-2013-002945

CR-2012-001459 CR-2012-008548 CR-2013-002969

CR-2012-001614 CR-2012-008816

Miscellaneous

ACE for CR-2011-006930

Attachment

A-7

ACE for CR-2012-002176

Eval-NMP-PRM-03046, (a)(1) Evaluation for 1-PRM-F01

Unit 1 Containment Spray System Health Report, 1st Quarter 2013

Unit 1 Neutron Monitoring System Health Report, 1st Quarter 2013

Unit 1 Service Water System Health Report, 1st Quarter 2013

Unit 2 High-Pressure Core Spray System Health Report, 1st Quarter 2013

Section 1R13: Maintenance Risk Assessments and Emergent Work Control

Procedures

CNG-MN-4.01-1004, On-Line T-Week Process, Revision 00302

N2-ISP-LDS-Q010, Reactor Building General Area Temperature Instrument Channel Functional

Test, Revision 00102

N2-OP-71D, Uninterruptible Power Supplies, Revision 00800

N2-SOP-29.1, Reactor Recirculation Pump Seal Failure, Revision 00101

N2-SOP-97, Reactor Protection Systems Failures, Revision 00401

NIP-OUT-01, Shutdown Safety, Revision 03700

S-ODP-OPS-0122, Posting and Control of Protected Equipment during Online and Outage

Operations, Revision 00500

Condition Reports

CR-2013-002461

CR-2013-002916

CR-2013-002926

CR-2013-002958

CR-2013-002998

CR-2013-005021

CR-2013-005077

Work Orders

WO C90962110

WO C91488068

WO C90648733

Miscellaneous

Control Room Operator Logs for Tuesday April 16, 2013

NIP-OUT-01, Shutdown Safety, Revision 03700, Attachment 1, Shutdown Safety Contingency

Plan (or Equivalent), Contingency Plan No. N1R22-003

NIP-OUT-01, Shutdown Safety, Revision 03700, Attachment 1, Shutdown Safety Contingency

Plan (or Equivalent), Contingency Plan No. N1R22-004

NIP-OUT-01, Shutdown Safety, Revision 03700, Attachment 1, Shutdown Safety Contingency

Plan (or Equivalent), Contingency Plan No. N1R22-005

Outage Control Center Logs for Tuesday April 16, 2013

Work Control Center Turnover Sheet for April 16, 2013, Days to Night.

Section 1R15: Operability Determinations and Functionality Assessments

Procedures

CNG-OP-1.01-1002, Conduct of Operability Determinations/Functionality Assessments,

Attachment

A-8

Revision 00200

N1-IPM-092-100, SRM Detector Drive Maintenance and Limit Switch Calibration, Revision 00700

N1-OP-18, Service Water System, Revision 02902

N1-OP-38A, Source Range Monitor, Revision 02000

N1-ST-C5, Secondary Containment and Reactor Building Emergency Ventilation System

Operability Testing, Revision 01600

N1-ST-C6, Source Range Monitor Operability Test, Revision 01100

Condition Reports

CR-2013-002637 CR-2013-003186 CR-2013-003698

CR-2013-002945 CR-2013-003445 CR-2013-004481

CR-2013-002969 CR-2013-003504 CR-2013-005079

CR-2013-002978 CR-2013-003520 CR-2013-004807

CR-2013-003107 CR-2013-003548

CR- 2013-003116 CR-2013-003567

CR-2013-003124 CR-2013-003589

Drawing

RX-147741, 10HN-18 Refinery Pump Elevation, Revision 0

Documents

UFSAR Section VI-2.0, Secondary Containment, Revision 15

UFSAR Section VII-3.0, Emergency Ventilation System, Revision 18

UFSAR Section VII-B, Containment Spray System, Revision 18

UFSAR Section XVI-2.0, Containment Spray System, Revision 20

Section 1R18: Plant Modifications

Procedure

N2-EPM-GEN-V786, MOD Actuator and Damper PM, Revision 00700

Condition Reports

CR-2013-002334

CR-2013-002303

Drawing

ECN Number ECP-12-000616-CN-004 LR18047C

Work Order

WO C919733104

Miscellaneous

ECP 12-000616, Installation of Bubble Tight Damper (BV-210-36)

ECP 13-000167, Installation of Replacement Pump for Unit 1 Service Water Radiation Monitor

ECP 13-000347, Temporary Change to Plug Hand Wheel Connection for 2HVP*AOD5A

Section 1R19: Post-Maintenance Testing

Attachment

A-9

Procedures

CNG-MN-4.01-1008, Pre-/Post-Maintenance Testing, Revision 00100

N1-FST-FPP-C005, Ventilation/Smoke Purge System, Revision 00400

S-EPM-GEN-063, MOV Diagnostic Testing, Revision 00700

Condition Reports

CR-2013-003051

CR-2013-003251

CR-2013-004003

CR-2013-004052

CR-2013-004177

CR-2013-004212

CR-2013-004253

Drawings

C-19410-C, Elementary Wiring Diagram 4.16 kV Emergency Power Boards and Diesel

Generators (102 and 103 Power Circuits), Revision 28, Sheet 1,

C-22277-C, 4160 Volt Power Board 102 Connection Diagram Unit 2-1, Diesel Generator 102,

Revision 09, Sheet 1

C-19437-C, Elementary Wiring Diagram 600V, Power Board 161B Control Circuits, Revision 25,

Sheet 2

C-19437-C, Elementary Wiring Diagram 600V, Power Board 161B Control Circuits, Revision 25,

Sheet 6

C-19017-C, Emergency Cooling System P&I Diagram, Revision 55, Sheet 1

Work Orders

WO C91473955

WO C91474635

WO C91973104

WO C92264883

WO C92279163

WO C92279776

Miscellaneous

ECP-13-000420-015-9, Removal and Replacement of Existing Cable 102-33 from EDG102 to

Power Board 102, Revision 0000

ECP-12-000575, Standard Spec for Electrical Installation Activities at NMP1, Revision 21.00

N21036, Limitorque Type SMB and SB Instruction and Maintenance Manual, NMPCNO:

N2L20000VALVOP004

SPEC NMP1-325M,Section II, Penetration Seals, Revision 1

Section 1R20: Refueling and Other Outage Activities

Procedures

CNG-OP-3.01-1000, Reactivity Management, Revision 00800

Attachment

A-10

N1-FHP-27C, Core Shuffle, Revision 00603

N1-FHP-25, General Description of Fuel Moves, Revision 02301

N1-OP-43C, Plant Shutdown, Revision 01200

N1-RESP-9, SRM Operability for Core Alterations, Revision 00001

N1-ST-V3, Rod Worth Minimizer Operability Test APRM/IRM Overlap Verification, Revision

01300

Condition Report

CR-2013-002793

Tagout

TO-30-0224

Miscellaneous

RFO22 Fuel Movement Instructions

Section 1R22: Surveillance Testing

Procedures

N1-ISP-LRT-TYC, Type C Containment Isolation Valve Local Leak Rate Test, Revision 00900

N1-ST-C5, Secondary Containment and Reactor Building Emergency Ventilation System

Operability Test, Revision 01600

N1-ST-Q15, Condensate Transfer System Operability Test, Revision 00703

N1-ST-Q3, High-Pressure Coolant Injection Pump and Check Valve Operability Test,

Revision 01300

N1-TSP-201-001, Integrated Leak Rate Test of Primary Containment Type A Test, Revision

00600

N2-CSP-GEN-D100, Reactor Water/Auxiliary Water Chemistry Surveillance, Revision 00601

N2-ISP-LDS-Q010, Reactor Building General Area Temperature Instrument Channel Functional

Test, Revision 00103

N22-CSP-W@101, Weekly Conductivity Monitor Channel Check, Revision 1

S-CAD-CHE-101, Chemistry Sample Conduct, Revision 0100

Condition Reports

CR-2013-002788

CR-2013-002637

Drawings

C-18013-C, Reactor Building Heating and Ventilation System, Revision 33

C-18014-C, Reactor Containment (Drywell and Torus) Inert Gas N2 Purge and Fill Drywell

Cooling System, Revision 58

Work Orders

WO C91214116

WO C92182070

Attachment

A-11

Miscellaneous

NUREG-1493, Performance-Based Containment Leak Test Program, September 1995

Section 1EP4: Emergency Action Level and Emergency Plan Changes

Procedures

EPIP-EPP-01, Classification of Emergency Conditions at Unit 1, Revision 23

EPIP-EPP-02, Classification of Emergency Conditions at Unit 2, Revision 22

EPMP-EPP-0101, Unit 1 Emergency Classification Technical Bases, Revision 01700

EPMP-EPP-0102, Unit 2 Emergency Classification Technical Bases, Revision 01900

Section 1EP6: Drill Evaluation

Procedure

EPIP-EPP-01, Classification of Emergency Conditions at Unit 1, Revision 02000

Section 2RS1: Radiological Hazard Assessment and Exposure Controls

Procedures

CNG-TR-1.01-1025, Radiation Protection Technician Training Program, Revision 00100

GAP-RPP-08, Control of High Locked High and Very High Radiation Areas, Revision 16

S-RAP-RPP-0103, Posting and Barricading Radiological Areas, Revision 02800

S-RAP-RPP-0201, Radiation Work Permit Initiation, Preparation, Control and Use,

Revision 02300

S-RAP-RPP-0801, High Locked High and Very High Radiation Area Monitoring and Control,

Revision 03000

S-RPIP-3.0, Radiological Surveys, Revision 01900

Condition Reports

CR-2013-002520

CR-2013-002781

CR-2013-003098

Audits, Self Assessments, and Surveillances

Q&PA Assessment Report 13-010, Assess Station Preparedness for Managing and Executing

N1R23

SA-2013-000005, Snapshot Assessment of 2012 4th Quarter Dose and Dose Rate Alarms

SA-2013-000034, Snapshot Assessment of Radiation Protection Job Hazard Analysis Process

Usage

Miscellaneous

BRAC Survey Trends in Discharge Piping Dose Rates, Unit 1, 1984 to 2013

BRAC Survey Trends in Recirc Suction Piping Dose Rates, Unit 1, 1984 to 2013

High Radiation Area/Locked High Radiation Area Gate Door Checklist, Unit 1, April 20, 2013

Personnel Qualification Form Verification, Employee Badge 38016, April 8, 2013

Personnel Qualification Form Verification, Employee Badge 38359, April 1, 2013

Personnel Qualification Form Verification, Employee Badge 4127, April 8, 2013

Personnel Qualification Form Verification, Employee Badge 4169, April 1, 2013

Personnel Qualification Form Verification, Employee Badge 4196, March 29, 2013

Attachment

A-12

Personnel Qualification Form Verification, Employee Badge 54337, February 25, 2013

RWP 113330H, RB 261 Reactor Water Cleanup Valve Work

RWP 113802H, Drywell Under-Vessel Work

RWP 113806H, Drywell In-Service Inspection

RWP 113810, Drywell General Scaffolding Activities

RWP 113815, RB 261 FAC In-Service Inspection

RWP 113890A, RB 340 Reactor Disassembly and Reassembly

RWP 113890B, RB 340 Underwater Work on Refuel Floor

RWP 113890E, RB 340 Reactor Cavity and Equipment Storage Pit Decon

RWP 113891, Spent Fuel Pool Gate Repair

Section 2RS2: Occupational ALARA Planning and Controls

Procedures

CNG-RP-1.01-1001, Station ALARA Committee, Revision 00000

CNG-RP-1.01-2003, Operational ALARA Planning and Controls, Revision 00000

N1-OP-34, Refueling Procedure (Includes Primary Chemistry Controls), Revision 03000

S-RAP-ALA-0101, Temporary Shielding, Revision 10

S-RAP-ALA-0102, ALARA Reviews, Revision 01500

Condition Reports

CR-2013-002267

CR-2013-003168

Self Assessment

SA-2012-000283, 4th Quarter 2012 ALARA Committee Effectiveness Review

Miscellaneous

5-Year Collective Radiation Exposure Reduction Plan, 2012 to 2016

ALARA Plan 2013-1-002, Drywell Under-Vessel Activities and Associated Activities N1R22,

April 10, 2013

ALARA Plan 2013-1-004, Drywell Operations and LLRT/ILRT Activities, April 10, 2013

ALARA Plan 2013-1-006, Drywell ISI Activities, April 10, 2013

ALARA Plan 2013-1-007, Recirc Pump Seals Replacement and Motor PMs (Numbers 11, 13 and

15), April 10, 2013

ALARA Plan 2013-1-010, Drywell Scaffold Activities, April 10, 2013

ALARA Plan 2013-1-014, Drywell Emergency Relief Valve and Pilot Valve Work Activities,

April 10, 2013

ALARA Plan 2013-1-024, Main Steam Isolation Valve 01-02 Stem Replacement Actuator

Remove/Replace and Testing, April 10, 2013

ALARA Plan 2013-1-029, Balance of Plant FAC Activities in RWCU HX Room and Valve Aisles,

April 10, 2013

ALARA Plan 2013-1-030, Refuel Floor Activities, dated April 10, 2013

ALARA Plan 2013-1-031, RWCU Miscellaneous Maintenance, PM, ST, Operations RFO 22,

April 10, 2013

ALARA Work In-Progress Review, 2013-1-006, Drywell ISI Activities, April 21, 2013

ALARA Work In-Progress Review, 2013-1-007, Recirc Pump Seals Replacement and Motor PMs,

April 22, 2013

ALARA Work In-Progress Review, 2013-1-010, Drywell Scaffold Activities, April 20, 2013

Attachment

A-13

ALARA Work In-Progress Review, 2013-1-011, Drywell Insulation, April 22, 2013

ALARA Work In-Progress Review, 2013-1-014, Drywell Emergency Relief Valve and Pilot Valve

Work Activities, April 22, 2013

ALARA Work In-Progress Review, 2013-1-024, Main Steam Isolation Valve 01-02 Stem

Replacement Actuator Remove/Replace and Testing, April 22, 2013

ALARA Work In-Progress Review, 2013-1-029, Balance of Plant FAC Activities in RWCU HX

Room and Valve Aisles, April 18, 2013

ALARA Work In-Progress Review, 2013-1-030, Refuel Floor Activities, April 20, 2013

Unit 1 Radiation Protection Pre-Outage Report, dated April 15, 2013

Section 2RS3: In-Plant Airborne Radioactivity Control and Mitigation

Procedures

GAP-RPP-04, Respiratory Protection Program, Revision 11

N1-RTP-76, Operation and Calibration of the Eberline PING-1A PING-1AMT Particulate Iodine

Noble Gas Monitor, Revision 02

S-RAP-RPP-0402, Selection and Issuance of Radiological Respiratory Protection Equipment,

Revision 12

S-RPIP-4.2, Respiratory Protection Quality Assurance Control Program, Revision 00200

S-RPIP-4.4, Maintenance Inspection and Testing of Respiratory Protection Equipment,

Revision 00700

S-RPIP-4.5, Use of Respiratory Protection Equipment, Revision 09

S-RPIP-6.0, Control and Use of HEPA Vacuum Cleaners and Portable HEPA Ventilation Units,

Revision 00300

Condition Reports

CR-2013-002816

CR-2013-002947

Self Assessment

SA-2011-000164, Radiological Respiratory Protection Program, November 18, 2011

Miscellaneous

Air Sample Unit 1 RB 340 Edge of Cavity, April 15, 2013, 5:43 a.m.

Air Sample Unit 1 RB 340 Edge of Cavity, April 15, 2013, 7:14 a.m.

Air Sample Unit 1 RB 340 Refuel Floor during Silver Dollar Installation, April 15, 2013, 9:20 p.m.

Air Sample Unit 1 RB 340 Refuel Floor during Stud Removal, April 17, 2013, 12:20 p.m.

HEPA Ventilation Log, dated April 23, 2013

Unit 1 System Health Report for 1st Quarter Control Room Ventilation, dated April 10, 2013

Unit 1 System Health Report for 1st Quarter RB Ventilation, dated April 10, 2013

Vacuum Cleaner Issue Log, dated April 23, 2013

Section 2RS4: Occupational Dose Assessment

Procedures

CNG-RP-1.01-2002 Effective Dose Equivalent - External, Revision 00000

CNG-RP-1.01-3002, Sampling and Analysis for 10 CFR 61 Waste Classification, Revision 00000

GAP-RPP-07, Internal and External Dosimetry Program, Revision 02100

S-RAP-ALA-0103, Dosimetry and Radiological Engineering Evaluations, Revision 00900

S-RPIP-4.6, DAC Hour Tracking and Estimating Internal Exposure, Revision 00500

Attachment

A-14

S-RPIP-5.5, Processing and Evaluating Personnel Contamination, Revision 01800

S-RPIP-5.7, Bioassay and Internal Dose Assessment, Revision 00900

S-RPIP-5.20, Dosimetry Program Quality Assurance, Revision 00800

S-RPIP-5.25, Exposure Evaluation Reports, Revision 01000

Condition Reports

CR-2013-002474

CR-2013-002678

CR-2013-002974

CR-2013-003247

CR-2013-003374

CR-2013-003350

CR-2013-003413

Miscellaneous

Oak Ridge Associated University E-mail Y. McCormick to A. Moisan RE: REIRS Data Verification,

dated April 1, 2013

Sentinel Report on Personnel with Dose Greater Than 400 mrem, dated April 22, 2013

S-RPIP-5.5 Attachment 1 Contamination Occurrence Report Number 1-13-RFO-003, dated

April 24, 2013

Section 2RS7: Radiological Environmental Monitoring Program

Procedures

CNG-EV-1.01-1000, Radiological Environmental Monitoring Program, Revision 001000

NLAP-ENV-400, Radiological Environmental Monitoring Program Land Use Census,

Inter-laboratory Comparison Program and Reporting, Revision 00.00

S-ENVSP-3, Radiological Sample Collection, Processing, and Shipment Land Use Census

Quality Control (Vendor Procedure), Revision 06.00

S-ENVSP-3.1, Milk Animal Census and Milk Sample Collection, Revision 01.00

S-ENVSP-3.2, Garden/Irrigation Census and Food Product (Vegetation and Irrigation Crop)

Sample Collection, Revision 02.00

S-ENVSP-3.3, Nearest Meat Animal Census and Meat, Poultry, and Egg Sample Collection,

Revision 01.00

S-ENVSP-3.4, Soil Sample Collection, Revision 01.00

S-ENVSP-3.5, Fish Sample Collection, Revision 01.00

S-ENVSP-3.6, Shoreline Sediment and Cladophora Sample Collection, Revision 01.00

S-ENVSP-3.7, Nearest Residence Census, Revision 00.00

S-ENVSP-4.1, TLD/OSL Preparation, Collection and Analysis, Revision 01400.00

S-ENVSP-4.2, Environmental Air Monitoring Sample Collection, Revision 01001.00

S-ENVSP-4.3, Environmental Air Monitoring Station Inspection and Maintenance,

Revision 00600.00

S-ENVSP-4.4, Environmental Surface Water Sample Collection and Compositing,

Revision 00900.00

S-ENVSP-12, Environmental Surveillance Quality Assurance/Quality Control Program,

Revision 001100.00

S-ENVSP-15, Sampling and Analysis for Unmonitored Pathways, Revision 01300.00

S-ENVSP-16, Sampling and Analysis of Monitoring Wells, Revision 00500.00

S-ENVSP-18, Environmental Data Review, Revision 01000.00

S-IPM-MET-001, Meteorological Monitoring System Equipment Check, Revision 00200.00

Attachment

A-15

S-IPM-MET-201, Dew Point Calibration, Revision 00100.00

S-IPM-MET-301, Barometric Pressure Calibration, Revision 03.00

S-IPM-MET-401, Precipitation Gauge Calibration, Revision 02.00

S-IPM-MET-601, Main Meteorological Tower 30 Foot Wind Speed and Direction Calibration,

Revision 00100.00

S-IPM-MET-602, Main Meteorological Tower 100 Foot Wind Speed and Direction Calibration,

Revision 00400.00

S-IPM-MET-603, Main Meteorological Tower 200 Foot Wind Speed and Direction Calibration,

Revision 00100.00

S-IPM-MET-611, Backup Meteorological Tower Wind Speed and Direction Calibration,

Revision 00200.00

S-IPM-MET-621, Inland Meteorological Tower Wind Speed and Direction Calibration,

Revision 00100.00

S-IPM-MET-701, Temperature and Delta Temperature Instrument Calibration,

Revision 00200.00

S-MET-ENV-01, Maintenance of Meteorological Monitoring Program, Revision 00100.00

S-MET-ENV-0002, Meteorological Data Verification and Edit, Revision 00600.00

S-MET-ENV-0003, Meteorological Monitoring Program Quality Assurance Quality Control,

Revision 00600.00

Condition Reports

CR-2012-000632 CR-2012-005817 CR-2012-010132

CR-2012-000664 CR-2012-006057 CR-2013-000603

CR-2012-000734 CR-2012-007114 CR-2013-001001

CR-2012-001143 CR-2012-007684

CR-2012-001488 CR-2012-009863

Work Orders

WO C91660878

WO C91875097

Audits, Self Assessments, and Surveillances

DTE Energy NAQA-12-0036, Audit 12-006 of Environmental Dosimetry Company, July 3, 2012

Entergy CR-LO-JAFLO-2012-00045, Radiological Environmental Monitoring Program Focused

Self Assessment, February 20 to 27, 2013

NUPIC Audit 22873, GEL Laboratories, LLC, Analytical Laboratory Services, December 13, 2011

Miscellaneous

2011 Annual Report, Meteorological Monitoring Program, Murray and Trettel, Inc., Palatine, IL

2012 Annual Quality Assurance Status Report, Environmental Dosimetry Company, dated

March 13, 2013

2012 Inter-laboratory Comparison Report, Eckert and Zeigler, dated March 29, 2013

2012 Land Use Census Summary Report, dated October 25, 2012

DVP-04.01, Environmental Laboratory Quality Assurance/Quality Control Program, Revision 4

EN-CY-102, Laboratory Analytical Quality Control, Revision 4

James A. FitzPatrick Environmental Laboratory Quality Assurance Report, January to

December 2011

Licensee Event Number 48901, Power Lost to Meteorological Instrumentation, dated April 9, 2013

Quality Assurance Topical Report, dated December 11, 2011

Attachment

A-16

Radiological Environmental Operating Report January to December, 2012, dated May 15, 2013

Radiological Engineering Evaluation Number C-99-011, Revision 7, 10 CFR 50.75(g) Record -

Unit 1 TB Roof Replacement, dated September 7, 2012

Radiological Engineering Evaluation Number C-99-011, Revision 8, 10 CFR 50.75(g) Record -

Elevated Tritium Concentration in Screen House In-Leakage, dated January 27, 2013

S-ENVSP-4.4 Attachment 5A L/S 7523 Sample Pump Control Setting Determination, Serial

Number L03004172, NRG Oswego Steam Station, dated August 14, 2009

S-ENVSP-4.4, Attachment 5A, L/S 7523 Sample Pump Control Setting Determination, Serial

Number L04004587, Unit 1 Intake Canal, dated April 20, 2009

S-ENVSP-4.4, Attachment 5A, L/S 7523 Sample Pump Control Setting Determination, Serial

Number L04004590, Unit 1 Intake Canal, dated April 20, 2009

Tektronix Certificate of Calibration 6776890, American Meter Mass Flow Meter Number 10429,

dated November 16, 2012

Tektronix Certificate of Calibration 6104009, American Meter Mass Flow Meter Number 10436,

dated April 20, 2012

Tektronix Certificate of Calibration 6780305, American Meter Mass Flow Meter Number 10458,

dated November 17, 2012

Tektronix Certificate of Calibration 6114558, American Meter Mass Flow Meter Number 10870,

dated April 23, 2012

Tektronix Certificate of Calibration 6380789, American Meter Mass Flow Meter Number 10899,

dated July 18, 2012

Unit 1 ODCM, Revision 34

Unit 1 Radioactive Effluent Release Report, January to December 2012, dated May 1, 2013

Unit 2 ODCM, Revision 35

Unit 2 UFSAR Chapter 2.3, Meteorology, Revision 19, October 2010

Section 4OA1: Performance Indicator Verification

Procedures

N2-CSP-GEN-D100, Reactor Water/Auxiliary Water Chemistry Surveillance, Revision 00601

N22-CSP-W@101, Weekly conductivity Monitor Channel Check, Revision 1

S-CAD-CHE-101, Chemistry Sample Conduct, Revision 01100

Miscellaneous

Nuclear Energy Institute 99-02, Regulatory Assessment Performance Indicator Guideline,

Revision 6

Section 4OA2: Problem Identification and Resolution

Procedures

CENG-AM-1.01-1005, Engineering Role and Responsibilities/Expectations, Revision 00303

CNG-CA-1.01-1004, Root Cause Analysis, Revision 00802

CNG-CA-2.01-1000, Self-Assessment and Benchmarking Process, Revision 00700

CNG-MN-4.01-1001, Work Order Execution and Closure Process, Revision 00401

CNG-MN-1.01-1000, Conduct of Maintenance, Revision 00200

N2-EMP-GEN-673, 24/48 VDC and 125 VDC Batteries - Cell and Connector Replacement,

Revision 00400

NPAP-INV-220, Storage and Handling of Material, Revision 01001

Nine Mile Point Station Policy Number 22, Work Document Quality, Revision 0

Attachment

A-17

Procedure Review Briefing Sheet CNG-HU-1.01-1001 HU Tools and Verification Process

Understanding Human Behavior and Error, Human Reliability Associates, David Embrey

Condition Reports

CR-1997-001696 CR-2012-000060 CR-2012-009469

CR-2001-005920 CR-2012-001137 CR-2012-010774

CR-2005-003461 CR-2012-001138 CR-2012-010907

CR-2007-007514 CR-2012-001139 CR-2013-001159

CR-2010-001220 CR-2012-001315 CR-2013-002102

CR-2010-001987 CR-2012-001316 CR-2013-002360

CR-2010-003899 CR-2012-002716 CR-2013-002443

CR-2010-007337 CR-2012-003724 CR-2013-003207

CR-2011-005737 CR-2012-004600 CR-2013-003357

CR-2011-007171 CR-2012-005362 CR-2013-005074

CR-2011-007269 CR-2012-005365 CR-2013-005117

CR-2011-007655 CR-2012-006030 CR-2013-005228

CR-2011-009896 CR-2012-006242 CR-2013-005235

CR-2011-010906 CR-2012-006823 CR-2013-005245

CR-2011-010953 CR-2012-007085

CR-2011-011006 CR-2012-007765

Drawings

3.N2.1-E21.1, One Line Diagram 125 VDC Control Bus, Revision 14

EE-1CA, One Line Diagram Emergency and Vital Bus Power Distribution Unit 2, Revision 14

EE-1CM, 125 VDC One Line Diagram Emergency Switchgear 2BYS*SWG002A, Revision 19

EE-1CN, 125 VDC One Line Diagram Emergency Switchgear 2BYS*SWG002B, Revision 17

EE-MO1F, Plant Master One Line Diagram Emergency and Normal 125V and 24/48VDC Unit 2,

Revision 8

Work Orders

WO C92017475

WO C92036878

Miscellaneous

CR Search for RCS*MOV18, Excessive Unidentified Leakage, and TS Required Shutdown for

January 1, 2000, until April 25, 2013

Design Engineering Request NM-2001-5894

Equipment Reliability Return to Excellence Plan

Equivalency Evaluation Number 00230 for RCS*MOV 10A&B and RCS*MOV 18A&B, dated

April 4, 2002

GE SIL No. 620, BWR 5 and 6 Reactor Recirculation System Pump Discharge Gate Valve

N2-ESP-BYS-Q767, Quarterly Battery Surveillance Test, completed on August 16 and 31, 2012;

February 11, March 7, and May 28, 2013

N2-ESP-BYS-R685, Divisions I, II, and III Battery Modified Profile Test, completed on April 4

and 10, 2010; April 16, July 25, and November 28, 2012

Root Cause Analysis, Cross-Cutting Theme Exists in the Aspect of Human Performance,

Resources, Documentation H.2(c) dated January 18, 2013

Root Cause Analysis, Unit 1 SCRAM due to Turbine Trip on May 2, 2011, dated

September 16, 2011

Attachment

A-18

Timeline of RCS*MOV 18A Problems

Unit 1 DEP System Health Report, 1st and 2nd Quarters 2013

Unit 2 DEP System Health Report, 1st and 2nd Quarters 2013

Valve Packing Data Sheet for RCS*MOV 10A and B

Valve Packing Data Sheet for RCS*MOV 18A and B

Vendor Manuals

35.40, Specifications Nuclear Class 1E Flooded Batteries GNB, dated August 2002

RS-1476, Stationary Battery and Vented Cell Installation and Operating Instructions C&D

Technologies, dated 2009

Calculation

EC-145, Verification of Adequacy of Division III Battery 2BYS*BAT2C, Revision 2

Section 4OA3: Follow-up of Events and Notices of Enforcement Discretion

Procedures

N1-OP-47A, 125 VDC Power System, Revision 02500

N1-SOP-47A.1, Loss of DC, Revision 00101

N1-SOP-6.1, Loss of SFP/RX Cavity Level/Decay Heat Removal, Revision 00501

N1-ST-R2, LOCA and EDG Simulated Auto Initiation Test, Revision 03201

N2-EMP-GEN-609, General Small Motor Maintenance, Revision 06

NIP-OUT-01, Shutdown Safety, Revision 03700

Condition Reports

CR-2013-001633

CR-2013-002916

CR-2013-002926

CR-2013-002958

CR-2013-002998

Miscellaneous

ACE for CR-2013-001633

CENG Safety Stand Down for April 16, 2013, Loss of Battery Bus 12 Event

Control Room Operator Logs for Tuesday, April 16, 2013

E191, NMPNS Specification for Safety-Related Motor Repairs, Revision 0

Outage Control Center Logs for Tuesday, April 16, 2013

PM Template for Small and Intermediate HP Motors

Unit 1 Station Alarm Log for Tuesday, April 16, 2013

Work Control Center Turnover Sheet for April 16, 2013, Days to Night

Attachment

A-19

LIST OF ACRONYMS

10 CFR Title 10 of the Code of Federal Regulations

AC alternating current

ADAMS Agencywide Documents Access and Management System

ALARA as low as reasonably achievable

ASME American Society of Mechanical Engineers

BWR boiling-water reactor

CAP corrective action program

CENG Constellation Energy Nuclear Group, LLC

DC direct current

ECCS emergency core cooling system

ECP engineering change package

EDG emergency diesel generator

ERV electro-matic relief valve

FA fire area

FAC flow accelerated corrosion

FCV flow control valve

HPCS high-pressure core spray

I&C instrumentation and control

IEEE Institute of Electrical and Electronics Engineers

IMC Inspection Manual Chapter

ISI inservice inspection

kV kilovolt

LER licensee event report

LOCA loss of coolant accident

LOOP loss of offsite power

NDE nondestructive examination

NCV non-cited violation

NMPNS Nine Mile Point Nuclear Station, LLC

NRC Nuclear Regulatory Commission

ODCM offsite dose calculation manual

psig pounds per square inch gauge

RB reactor building

RCIC reactor core isolation cooling

RCS reactor coolant system

REMP radiological environmental monitoring program

RG regulatory guide

RHR residual heat removal

RPT radiation protection technician

RPV reactor pressure vessel

RWCU reactor water cleanup

RWP radiation work permit

SDC shutdown cooling

SDP significance determination process

SFP spent fuel pool

SSC structure, system, and component

Enclosure

A-20

ST surveillance testing

TLD thermo luminescent dosimeter

TS technical specification

UFSAR Updated Final Safety Analysis Report

UT ultrasonic testing

VDC volts direct current

Attachment