ML22026A350

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Integrated Inspection Report 05000220/2021004 and 05000410/2021004
ML22026A350
Person / Time
Site: Nine Mile Point  Constellation icon.png
Issue date: 01/26/2022
From: Erin Carfang
NRC/RGN-I/DORS
To: Rhoades D
Exelon Generation Co LLC, Exelon Nuclear
Carfang E
References
IR 2021004
Download: ML22026A350 (22)


See also: IR 05000220/2021004

Text

January 26, 2022

Mr. David P. Rhoades

Senior Vice President

Exelon Generation Company, LLC

President and Chief Nuclear Officer

Exelon Nuclear

4300 Winfield Road

Warrenville, IL 60555

SUBJECT: NINE MILE POINT NUCLEAR STATION, UNITS 1 AND 2 - INTEGRATED

INSPECTION REPORT 05000220/2021004 AND 05000410/2021004

Dear Mr. Rhoades:

On December 31, 2021, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at Nine Mile Point Nuclear Station, Units 1 and 2. On January 20, 2022, the NRC

inspectors discussed the results of this inspection with Mr. Adam Schuerman, Plant Manager,

and other members of your staff. The results of this inspection are documented in the enclosed

report.

One finding of very low safety significance (Green) is documented in this report. This finding

involved a violation of NRC requirements. We are treating this violation as a non-cited violation

(NCV) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violation or the significance or severity of the violation documented in this

inspection report, you should provide a response within 30 days of the date of this inspection

report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional

Administrator, Region I; the Director, Office of Enforcement; and the NRC Resident Inspector at

Nine Mile Point Nuclear Station, Units 1 and 2.

D. Rhoades 2

This letter, its enclosure, and your response (if any) will be made available for public inspection

and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document

Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public

Inspections, Exemptions, Requests for Withholding.

Sincerely,

Digitally signed by Erin E.

Erin E. Carfang Carfang

Date: 2022.01.26 13:19:19

-05'00'

Erin E. Carfang, Chief

Projects Branch 1

Division of Operating Reactor Safety

Docket Nos. 05000220 and 05000410

License Nos. DPR-63 and NPF-69

Enclosure:

As stated

cc w/ encl: Distribution via LISTSERV

ML22026A350

x Non-Sensitive x Publicly Available

x SUNSI Review

Sensitive Non-Publicly Available

OFFICE RI/DORS RI/DORS RI/DORS

NAME GStock JHawkins ECarfang

DATE 1/26/22 1/26/22 1/26/22

U.S. NUCLEAR REGULATORY COMMISSION

Inspection Report

Docket Numbers: 05000220 and 05000410

License Numbers: DPR-63 and NPF-69

Report Numbers: 05000220/2021004 and 05000410/2021004

Enterprise Identifier: I-2021-004-0115

Licensee: Exelon Generation Company, LLC

Facility: Nine Mile Point Nuclear Station

Location: Oswego, NY

Inspection Dates: October 1, 2021 to December 31, 2021

Inspectors: G. Stock, Senior Resident Inspector

C. Kline, Resident Inspector

B. Sienel, Resident Inspector

J. Demarshall, Senior Operations Engineer

T. Fish, Senior Operations Engineer

J. Hawkins, Senior Project Engineer

P. Ott, Operations Engineer

Approved By: Erin E. Carfang, Chief

Projects Branch 1

Division of Operating Reactor Safety

Enclosure

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees

performance by conducting an integrated inspection at Nine Mile Point Nuclear Station, Units 1

and 2, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the

NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer

to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Failure to Correct a Condition Adverse to Quality with an Uninterruptible Power Supply

Cornerstone Significance Cross-Cutting Report

Aspect Section

Mitigating Green None (NPP) 71152

Systems NCV 05000220,05000410/2021004-01

Open/Closed

The inspectors documented a self-revealed Green non-cited violation (NCV) of Title 10 of the

Code of Federal Regulations (10 CFR) Part 50, Appendix B, Criterion XVI, Corrective Action,

when Exelon did not ensure that a condition adverse to quality (CAQ) associated with an

identified deviation from the normal operating frequency of an uninterruptible power supply

(UPS) was promptly identified and corrected. Specifically, on August 1, 2016, after performing

maintenance on and placing the UPS-162A in service, Exelon documented an off-normal

condition related to the UPS inverter frequency being lower than normal and oscillating.

Exelon closed this issue report (IR) to trend without properly evaluating and correcting the

condition, resulting in the failure of the reactor protection system (RPS) UPS-162A and

causing the plant to experience a half-scram condition, an isolation of both emergency

condensers, and an isolation of the reactor water cleanup (RWCU) system on September 25,

2021.

Additional Tracking Items

Type Issue Number Title Report Section Status

LER 05000220/2021001-00 LER 2021-001-00, Average 71153 Closed

Power Range Monitors

Declared Inoperable Due to

Trip of Reactor Recirculation

Pump 13

LER 05000220/2021002-00 LER 2021-002-00, Isolation 71153 Closed

of Both Emergency

Condensers Due to Loss of

UPS-162A

2

PLANT STATUS

Unit 1 began the inspection period at rated thermal power. On October 2, 2021, reactor power

was reduced to approximately 75 percent for a control rod pattern adjustment, control rod scram

time testing, and turbine valve testing and returned to rated thermal power the same day. On

November 2, 2021, reactor power was reduced to approximately 98 percent to maintain inlet to

discharge differential temperature within state limits due to condenser fouling. On

November 13, 2021, reactor power was reduced to approximately 51 percent to correct the

condenser fouling. On November 13, 2021, Unit 1 was returned to rated thermal power. Unit 1

remained at or near rated thermal power for the remainder of the inspection period.

Unit 2 began the inspection period at rated thermal power. On October 9, November 21, and

December 10, 2021, reactor power was reduced to approximately 75 percent to perform control

rod channel interference testing, control rod scram time testing, and control rod pattern

adjustments. In each instance, Unit 2 was returned to rated thermal power on the same day or

the following day and remained at or near rated thermal power for the remainder of the

inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in

effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with

their attached revision histories are located on the public website at http://www.nrc.gov/reading-

rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared

complete when the IP requirements most appropriate to the inspection activity were met

consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection

Program - Operations Phase. The inspectors performed activities described in IMC 2515,

Appendix D, Plant Status, conducted routine reviews using IP 71152, Problem Identification

and Resolution, observed risk significant activities, and completed on-site portions of IPs. The

inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel to assess licensee performance and compliance with Commission rules and

regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Seasonal Extreme Weather Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated readiness for seasonal extreme weather conditions prior to

the onset of seasonal cold temperatures for the Unit 1 emergency diesel generators

and the Unit 2 Division I and II diesel generators.

Impending Severe Weather Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated the adequacy of the overall preparations to protect risk-

significant systems from impending severe weather for high winds on

December 6, 2021.

3

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following

systems/trains:

(1) Unit 2 control rod drive on November 23, 2021

(2) Unit 2 Division II residual heat removal on November 23, 2021

(3) Unit 2 Division II diesel generator on November 29, 2021

(4) Unit 2 reactor building closed loop cooling water on November 29, 2021

Complete Walkdown Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated system configurations during a complete walkdown of the

Unit 2 standby gas treatment system on November 4, 2021.

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (8 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a

walkdown and performing a review to verify program compliance, equipment functionality,

material condition, and operational readiness of the following fire areas:

(1) Unit 2 reactor building 175' and 240', reactor core isolation cooling pump room, fire

area 2, on October 5, 2021

(2) Unit 2 reactor building 261', standby gas treatment rooms A and B, fire areas 4, 73,

and 74, on November 4, 2021

(3) Unit 2 Division I switchgear room, fire area 17, on November 22, 2021

(4) Unit 2 Division II diesel generator control room, fire area 29, on November 23, 2021

(5) Unit 2 reactor building 328, fire areas 34 and 35, on November 30, 2021

(6) Unit 2 Division III diesel generator control room 261/274', fire area 30, on

December 13, 2021

(7) Unit 2 Division I diesel generator control room 261/274', fire area 28, on

December 13, 2021

(8) Unit 2 control building 288' relay room, fire area 24, on December 14, 2021

71111.06 - Flood Protection Measures

Inspection Activities - Internal Flooding (IP Section 03.01) (1 Sample)

The inspectors evaluated internal flooding mitigation protections in the:

(1) Unit 2 Division I and II emergency switchgear rooms, on November 22, 2021

4

71111.11A - Licensed Operator Requalification Program and Licensed Operator Performance

Requalification Examination Results (IP Section 03.03) (2 Samples)

(1) The inspectors reviewed and evaluated the licensed operator examination failure

rates for the requalification annual operating exam administered

October - November 2021.

(2) The inspectors reviewed and evaluated the Unit 1 licensed operator annual

requalification results for the annual operating exam on December 6, 2021.

71111.11B - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Requalification Program (IP Section 03.04) (1 Sample)

(1) Biennial Requalification Written Examinations

The inspectors evaluated the quality of the licensed operator biennial requalification

written examination administered October - November 2021.

Annual Requalification Operating Tests

The inspectors evaluated the adequacy of the facility licensees annual requalification

operating test.

Administration of an Annual Requalification Operating Test

The inspectors evaluated the effectiveness of the facility licensee in administering

requalification operating tests required by 10 CFR 55.59(a)(2) and that the facility

licensee is effectively evaluating their licensed operators for mastery of training

objectives.

Requalification Examination Security

The inspectors evaluated the ability of the facility licensee to safeguard examination

material, such that the examination is not compromised.

Remedial Training and Re-examinations

The inspectors evaluated the effectiveness of remedial training conducted by the

licensee, and reviewed the adequacy of re-examinations for licensed operators who

did not pass a required requalification examination.

Operator License Conditions

The inspectors evaluated the licensees program for ensuring that licensed operators

meet the conditions of their licenses.

5

Control Room Simulator

The inspectors evaluated the adequacy of the facility licensees control room

simulator in modeling the actual plant, and for meeting the requirements contained in

10 CFR 55.46.

Problem Identification and Resolution

The inspectors evaluated the licensees ability to identify and resolve problems

associated with licensed operator performance.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01)

(2 Samples)

(1) The inspectors observed Unit 1 operations personnel during a planned reactor

downpower to approximately 80 percent for a rod pattern adjustment and control rod

scram time testing on October 1, 2021.

(2) The inspectors observed Unit 2 operations personnel during a planned reactor

downpower to approximately 97 percent and control rod friction testing on

October 8, 2021.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (2 Samples)

(1) The inspectors observed a Unit 2 simulator evaluation that included the loss of an

emergency switchgear bus, a trip of a feedwater heater drain pump, a failure to

SCRAM, and a loss of coolant accident inside containment on October 12, 2021.

(2) The inspectors observed a Unit 1 annual examination that included an unplanned

opening of an electro-matic relief valve, the 12 emergency condenser tube leak, an

instrument air leak, and a steam leak inside containment on October 26, 2021.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (3 Samples)

The inspectors evaluated the effectiveness of maintenance to ensure the following

structures, systems, and components (SSCs) remain capable of performing their intended

function:

(1) Unit 1 safety-related ventilation control room chiller 11B oil leak

(2) Unit 2 automatic depressurization system makeup valve stuck open

(3) Unit 2 service water discharge valve failure to open

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the

following planned and emergent work activities to ensure configuration changes and

appropriate work controls were addressed:

6

(1) Unit 2 elevated risk during scheduled high pressure core spray maintenance on

October 26, 2021

(2) Unit 1 elevated risk during scheduled 12 feedwater pump maintenance on

November 3, 2021

(3) Unit 2 elevated risk during unplanned reactor core isolation cooling maintenance on

November 9, 2021

(4) Unit 2 elevated risk during scheduled Division I emergency diesel generator 6-year

preventive maintenance on November 17, 2021

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (5 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the

following operability determinations and functionality assessments:

(1) Unit 1 emergency diesel generator 102 due to inaccurate day tank level indication on

October 5, 2021

(2) Unit 1 11 and 12 emergency cooling systems following isolation during the loss of

reactor protection system 11 on October 15, 2021

(3) Unit 2 Division III diesel generator due to potential fuel oil lubricity out of specification

on October 18, 2021

(4) Unit 2 Division II diesel generator following jacket water leak on November 3, 2021

(5) Unit 2 reactor core isolation cooling due to flow controller failure on

November 8, 2021

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02)

(1 Sample)

The inspectors evaluated the following temporary or permanent modifications:

(1) Permanent Modification: ECP-21-000437, Unit 2 Division II Emergency Diesel

Generator Governor Booster Modification

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the following post-maintenance test activities to verify system

operability and functionality:

(1) Unit 2 Division II diesel generator governor replacement on November 6, 2021

(2) Unit 2 Division I control building chiller maintenance on December 2, 2021

(3) Unit 1 121 core spray pump and booster pump breaker replacements on

December 2, 2021

(4) Unit 2 reactor core isolation cooling following flow controller maintenance on

November 10, 2021

7

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Surveillance Tests (other) (IP Section 03.01) (2 Samples)

(1) N1-ST-Q8A, Liquid Poison 11 and Check Valve Operability Test, on

October 18, 2021

(2) N2-ISP-CSL-Q001, Low Pressure Core Spray Pump Discharge Flow - Low (Bypass)

Instrument Channel Functional Test, on December 21, 2021

RCS Leakage Detection Testing (IP Section 03.01) (1 Sample)

(1) N2-OSP-LOG-S001, Shift Checks - Mode 1, on November 29, 2021

71114.06 - Drill Evaluation

Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01)

(1 Sample)

(1) The inspectors evaluated a Unit 2 simulator evaluation which included a failure to

SCRAM, a loss of coolant accident, and the declaration of an Alert on

October 12, 2021.

OTHER ACTIVITIES - BASELINE

71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

MS08: Heat Removal Systems (IP Section 02.07) (2 Samples)

(1) Unit 1 - October 1, 2020 through September 30, 2021

(2) Unit 2 - October 1, 2020 through September 30, 2021

MS09: Residual Heat Removal Systems (IP Section 02.08) (2 Samples)

(1) Unit 1 - October 1, 2020 through September 30, 2021

(2) Unit 2 - October 1, 2020 through September 30, 2021

MS10: Cooling Water Support Systems (IP Section 02.09) (2 Samples)

(1) Unit 2 - October 1, 2020 through September 30, 2021

(2) Unit 1 - October 1, 2020 through September 30, 2021

71152 - Problem Identification and Resolution (PI&R)

Semiannual Trend Review (IP Section 02.02) (1 Sample)

(1) The inspectors reviewed the licensees corrective action program for potential

adverse trends that might be indicative of a more significant safety issue.

8

Annual Follow-up of Selected Issues (IP Section 02.03) (2 Samples)

The inspectors reviewed the licensees implementation of its corrective action program

related to the following issues:

(1) IR 04448532 - Review of Uninterruptible Power Supply Failure

(2) IR 04372127 - Review of Trend in Surveillance Test Interval Implementation

71153 - Follow Up of Events and Notices of Enforcement Discretion

Event Report (IP Section 03.02) (2 Samples)

The inspectors evaluated the following licensee event reports (LERs):

(1) LER 05000220/2021-001-00, Average Power Range Monitors Declared Inoperable

Due to Trip of Reactor Recirculation Pump 13. (ADAMS Accession

No. ML21144A050). The inspectors determined that it was not reasonable to foresee

or correct the cause discussed in the LER, therefore no performance deficiency was

identified. The inspectors did not identify a violation of NRC requirements. This LER

is closed.

(2) LER 05000220/2021-002-00, Isolation of Both Emergency Condensers Due to Loss

of UPS-162A. (ADAMS Accession No. ML21327A024). The inspection conclusions

associated with this LER are documented in this report under Inspection Results. This

LER is closed.

INSPECTION RESULTS

Failure to Correct a Condition Adverse to Quality with an Uninterruptible Power Supply

Cornerstone Significance Cross-Cutting Report

Aspect Section

Mitigating Green None (NPP) 71152

Systems NCV 05000220,05000410/2021004-01

Open/Closed

The inspectors documented a self-revealed Green non-cited violation (NCV) of Title 10 of the

Code of Federal Regulations (10 CFR) Part 50, Appendix B, Criterion XVI, Corrective

Action, when Exelon did not ensure that a condition adverse to quality (CAQ) associated with

an identified deviation from the normal operating frequency of an uninterruptible power supply

(UPS) was promptly identified and corrected. Specifically, on August 1, 2016, after performing

maintenance on and placing the UPS-162A in service, Exelon documented an off-normal

condition related to the UPS inverter frequency being lower than normal and oscillating.

Exelon closed this issue report (IR) to trend without properly evaluating and correcting the

condition, resulting in the failure of the reactor protection system (RPS) UPS-162A and

causing the plant to experience a half scram condition, an isolation of both emergency

condensers, and an isolation of the reactor water cleanup (RWCU) system on September 25,

2021.

Description: In 1993, motor generator sets at Unit 1 were replaced with four safety-related

UPSs (UPS-162A and -B, UPS-172A and -B) to supply conditioned 120 VAC power to the

RPS and instrument buses. Preventive maintenance is performed on the Unit 1 internal UPS

circuit cards by replacing them every 10 years.

9

On September 25, 2021, UPS-162A experienced voltage and frequency perturbations

(-5 VAC and 0.2 Hz from the normal values) which resulted in actuation of the RPS bus 11

under frequency protective relaying. This actuation caused a loss and subsequent restoration

of RPS bus 11 on UPS-162A which resulted in a half scram, an isolation of both emergency

condensers, and RWCU isolation. After troubleshooting the equipment and consulting with

the vendor, Exelon determined a capacitor, as well as an oscillator and sync circuit card,

required replacement. Exelon replaced these components, sent them for failure analysis, and

restored the UPS to service.

On October 28, 2021, Exelon completed a corrective action program evaluation (CAPE)

under IR 04448532. This evaluation ruled out the capacitor as a cause of the UPS failure.

Exelon determined that the cause of the failure was a premature failure of the UPS-162A

oscillator and sync circuit card. The evaluation found that the circuit card issue had potentially

existed since the UPS circuit cards were last replaced and placed in service in July 2016.

Exelons CAPE documented that two days after placing the UPS in-service, IR 02699078 was

written for observed UPS-162A frequency oscillations of 0.2 Hz and a lower than expected

voltage. This IR was closed with no additional actions taken to troubleshoot or correct the

abnormal condition. Exelons CAPE determined that the organization failed to adequately

address the documented frequency oscillations and generate a work order to investigate and

repair the condition. Exelon also determined that procedure N1-EPM-UPS-003, UPS

Maintenance PM, was inadequate to address frequency oscillations and that system internal

and external operating experience (OPEX) reviews were inadequate. Exelon received the

vendor failure analysis report (FAR 21-005) on November 15, 2021. This report concluded, in

part, that the failed oscillator and sync boards caused the inverter to phase drift and the UPS

to lose sync within 15 minutes when temperatures exceeded 105 degrees Fahrenheit, as

opposed to the normal temperature rating of 120 degrees Fahrenheit.

The inspectors reviewed Exelons CAPE, failure analysis report, and procedures. Exelons IR

02699078, which documented the observed frequency oscillations in 2016, also documented

Recommended Actions to determine if oscillations can lead to a fault in the UPS (could

lead to a loss of RPS 11). The inspectors found no documented answer to the recommended

action above. The Functional Basis section of the IR states, The fluctuation (0.25 Hz) is

within the acceptance criteria for N1-EPM-UPS-003 (59.7-60.3 Hz). A walkdown was

performed by EMD [electrical maintenance] and they did not identify an immediate concern

with functionality. UPS-162A remains functional. However, Exelons CAPE concluded that

procedure N1-EPM-UPS-003 was inappropriately used to determine the functionality of

UPS-162A, specifically that frequency oscillations, whether in the acceptance criteria band or

not, are an abnormal condition and should not be accepted under any circumstance, as this is

a sign of degradation and potential premature failure. The inspectors also noted that Exelon

procedure PI-AA-120, "Issue Identification and Screening Process," Revision 11, Section

4.4.6, states, in part, to determine if the as-found operability and functionality of any system,

structure, or component is affected by the condition and document the basis of the

determination. Section 4.6.6 states, in part, to determine if any additional actions are

necessary and route the issue to the responsible department to create actions.

Based on the information above, the inspectors determined that Exelon did not ensure that a

CAQ associated with an identified deviation from the normal operating frequency of

UPS-162A was promptly identified and corrected. Specifically, after performing maintenance

and placing the UPS in service, Exelon documented an off-normal condition related to the

UPS inverter frequency being lower than normal and oscillating yet closed this IR without

properly evaluating and correcting the condition.

10

Corrective Actions: Exelon replaced the failed UPS oscillator and sync circuit cards, revised

UPS maintenance procedures, added frequency oscillation observation to the system

walkdown checklist, sent the failed circuit cards out for failure analysis, and generated a crew

learning for timely OPEX reviews.

Corrective Action References: IR 04446321

Performance Assessment:

Performance Deficiency: Exelon's failure to ensure that a CAQ associated with an identified

deviation from the normal operating frequency of UPS-162A was promptly identified and

corrected is a performance deficiency that was within Exelons ability to foresee and correct,

and which should have been prevented.

Screening: The inspectors determined the performance deficiency was more than minor

because it was associated with the Design Control attribute of the Mitigating Systems

cornerstone and adversely affected the cornerstone objective to ensure the availability,

reliability, and capability of systems that respond to initiating events to prevent undesirable

consequences. Specifically, Exelon not ensuring that a CAQ associated with a safety-related

UPS was promptly identified and corrected resulted in reduced UPS reliability, a half-scram

condition, an isolation of both emergency condensers, and an isolation of the RWCU system.

Significance: The inspectors assessed the significance of the finding using Appendix A, The

Significance Determination Process (SDP) for Findings At-Power. Using Exhibit 2 of

Appendix A, the inspectors determined this finding was of very low safety significance

(Green) because Yes was not answered to any of the screening questions.

Cross-Cutting Aspect: Not Present Performance. No cross-cutting aspect was assigned to

this finding because the inspectors determined the finding did not reflect present licensee

performance.

Enforcement:

Violation: 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requires, in part,

that measures shall be established to ensure that CAQs, such as deviations and

nonconformances are promptly identified and corrected. Exelons procedure PI-AA-120,

"Issue Identification and Screening Process," states, in part, for CAQ to determine if the as-

found operability and functionality of any system, structure, or component is affected by the

condition and document the basis of the determination. The procedure also states to

determine if any additional actions are necessary and route the issue to the responsible

department to create actions.

Contrary to the above, between August 1, 2016, and September 25, 2021, Exelon did not

ensure that a CAQ associated with an identified deviation from the normal operating

frequency of UPS-162A was promptly identified and corrected. Specifically, on August 1,

2016, after performing maintenance and placing the UPS in service, Exelon documented an

off-normal condition related to the UPS inverter frequency being lower than normal and

oscillating but closed this IR without properly evaluating and correcting the condition resulting

in the failure of the RPS UPS-162A and caused the plant to experience a half-scram

condition, an isolation of both emergency condensers, and an isolation of the RWCU system.

Enforcement Action: This violation is being treated as an NCV, consistent with Section 2.3.2

of the Enforcement Policy.

11

Minor Performance Deficiency 71152

Minor Performance Deficiency: The inspectors reviewed a CAPE completed by Exelon staff,

and their identified corrective actions, following a series of issues in the implementation of the

surveillance frequency control program, including a missed surveillance as a result of an

inadequate evaluation. The missed surveillance was for the calibration of Unit 1 remote

shutdown panel reactor vessel water level indication in accordance with the surveillance

frequency control program. Exelons CAPE included an extent of condition review of all

completed surveillance frequency changes to ensure no other technical flaws

existed. Corrective actions included ensuring future surveillance frequency changes are

routed through regulatory assurance to verify the procedures align with the appropriate

technical specification surveillance requirements. Exelon also established a checklist to be

performed during the development of future surveillance frequency changes that includes the

steps required to avoid missed surveillances.

The inspectors reviewed the evaluation, extent of condition review, and relevant IRs and

interviewed the surveillance frequency control program owner. Based on the documents

reviewed and discussions with personnel, the inspectors determined Exelons evaluation of

the issue was adequate and provided for corrective action commensurate with the safety

significance of the problem. Exelon's failure to perform the missed surveillance discussed

above in the required timeframe is a performance deficiency.

Screening: The inspectors determined the performance deficiency was minor. The inspectors

evaluated the missed surveillance for significance in accordance with the guidance in IMC 0612, Appendix B, "Issue Screening," and Appendix E, "Examples of Minor Issues." The

performance deficiency was minor because it did not adversely affect a cornerstone objective

and following identification an appropriate risk assessment was developed and the

surveillance successfully completed in accordance with Technical Specification Surveillance

Requirement 4.0.3.

Significance: The inspectors assessed the significance of the finding using Appendix A, The

Significance Determination Process (SDP) for Findings At-Power. This performance

deficiency was of minor significance and, therefore, are not subject to enforcement action in

accordance with the NRC's Enforcement Policy.

Minor Performance Deficiency 71152

Minor Performance Deficiency: The inspectors performed a review of a recent UPS failure

that occurred at Unit 1 on September 25, 2021. Exelons CAPE, under IR 04448532,

documented that UPS-162A experienced voltage and frequency perturbations (-5 VAC and

0.2 Hz from the normal values) which resulted in actuation of the RPS bus 11 underfrequency

protective relaying. This actuation caused a loss and subsequent restoration of RPS bus 11

on UPS-162A which resulted in a half SCRAM, an isolation of both emergency condensers,

and RWCU isolation. The inspectors reviewed this CAPE to assess Exelons ability to

adequately identify problems, evaluate the causes of the equipment issues, and resolve the

issues in a timely manner.

During the review, the inspectors noted one more than minor performance deficiency (PD)

which is documented separately as an NCV in this report, and one minor PD, which is

documented below.

12

Minor PD: Exelon procedure PI-AA-115, "Operating Experience Program," Revision 5,

Section 4 for the receipt, screening, and processing of OPEX documents states, in part, to

perform an initial screening to determine the appropriate OPEX evaluation significance,

initiate an IR as applicable in Attachment 1, or if there is potentially new information that

challenges the conservatism of current external event design assumptions, and retain

relevant OPEX information in the ENGAGE Health notebooks in accordance with procedure

ER-AA-2030, "Conduct of Equipment Reliability Manual." Procedure ER-AA-2030, Section

4.3.4 for OPEX and peer lessons learned states, in part, that engineers should read daily

industry OPEX reports, review similar station IRs, and perform periodic OPEX searches on

industry websites. In addition, the procedure discusses that the ENGAGE Health notebooks

is where relevant OPEX should be retained and at a minimum updated semiannually.

Attachment 2 of this procedure goes on to state that the engineer is responsible for initial

OPEX reviews and the generation of IRs for required Level 3 OPEX reviews.

Contrary to these procedures, the inspectors found that Exelons CAPE determined that, The

OPEX reviews documented in Engage Health for this system appear to be inadequate. More

robust OPEX reviews may have allowed the frequency oscillations to be identified as a

potential failure mechanism earlier. This contributed to the failure in this event. The

inspectors noted that the CAPE generated an action to generate a crew learning for timely

OPEX reviews. Based on the external OPEX and the lack reviews and retention of the OPEX

for the UPS system, the inspectors questioned Exelon about whether a "crew learning" was

enough to correct this deficiency. The inspectors determined that the "crew learning" was an

action that could correct the OPEX review and retention issues going forward but that the

potential OPEX gap could remain unless system engineers conducted a "look back" to

ensure previous OPEX was accurately captured. Exelon documented this in IR 04448532.

Significance: The inspectors assessed the significance of the finding using Appendix A, The

Significance Determination Process (SDP) for Findings At-Power.

Observation: Semi-Annual Trend 71152

The inspectors evaluated a sample of issues and events that occurred from July 2021

through December 2021 to determine whether issues were appropriately considered as

emerging or adverse trends. The inspectors verified issues were appropriately evaluated by

Exelon staff for potential trends and addressed within the scope of the corrective action

program or through department review.

The inspectors did not identify any new trends that could indicate a more significant safety

issue. Exelon documented a trend in critical component failures during this evaluation

period. This included the failure of the Unit 1 12 high pressure coolant injection controller,

loss of RPS 11 following the failure of UPS-162A, the Unit 2 'C' service water pump discharge

valve failure to open, and Division II emergency diesel generator jacket water leak. These

issues were captured in trend IR 04459468 which resulted in Exelon personnel performing a

work group evaluation for commonalities between the failures. Exelon also identified several

instances of rework associated with supplemental workforce over a short period of time and

documented a potential trend in IR 04439810. None of these cases resulted in inoperability or

unavailability of safety systems. The inspectors also noted other minor potential adverse

trends identified by Exelon staff in the areas of equipment challenges in both units' instrument

air systems and failures of fire detectors at both units requiring additional walkdowns and

patrols.

13

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On January 20, 2022, the inspectors presented the integrated inspection results to

Mr. Adam Schuerman, Plant Manager, and other members of the licensee staff.

THIRD PARTY REVIEWS

Inspectors reviewed the World Association of Nuclear Operators report that was issued during

the inspection period.

14

DOCUMENTS REVIEWED

Inspection Type Designation Description or Title Revision or

Procedure Date

71111.01 Corrective Action 04198397

Documents 04445508

04461612

Procedures N1-OP-64 Meteorological Monitoring 02100

N2-OP-102 Meteorological Monitoring 02800

OP-AA-108-111 Severe Weather and Natural Disaster Guidelines 023

Work Orders C93760254

C93762635

C93805503

71111.04 Drawings PID-11D Piping and Instrumentation Diagram Service Water System 12

PID-13A Piping and Instrumentation Diagram Reactor Building 19

Closed Loop Cooling Water

PID-30A Piping and Instrumentation Diagram Control Rod Drive 29

Hydraulic System

PID-30B Piping and Instrumentation Diagram Control Rod Drive 14

Hydraulic System

PID-30C Piping and Instrumentation Diagram Control Rod Drive 15

Hydraulic System

PID-31A Piping and Instrumentation Diagram Residual Heat 27

Removal System

PID-43G Piping and Instrumentation Diagram Fire Protection - 28

Water

PID-61B Piping and Instrumentation Diagram Primary Containment 23

Purge and Standby Gas Treatment

PID-61C Piping and Instrumentation Diagram Primary Containment 8

Purge and Standby Gas Treatment

Miscellaneous Green NCV Failure to Ensure Proper Control of the Standby Gas

05000410/2018002- Treatment System Damper Valve, 2GTS-V2000, Within

01 Procedures, Materials, and Design Controls

Procedures N2-OP-13 LINEUPS, Reactor Building Closed Loop Cooling System 004

N2-OP-30 Control Rod Drive 26

N2-OP-31 Residual Heat Removal System 036T1

15

Inspection Type Designation Description or Title Revision or

Procedure Date

N2-OP-61B Standby Gas Treatment 17

N2-OP-61B- Standby Gas Treatment - LINEUPS 0100

LINEUPS

PID-31B Piping and Instrumentation Diagram Residual Heat 23

Removal System

PID-31C Piping and Instrumentation Diagram Residual Heat 17

Removal System

PID-31E Piping and Instrumentation Diagram Residual Heat 21

Removal System

71111.05 Drawings PID - 43G Charcoal Bed Deluge System 28

Fire Plans N2-FPI-PFP-0201 Station Fire Protection Instruction 06

N2-PFP-CB261 Control Building, El 261/274 0

N2-PFP-CB288 Control Building, El 288 0

N2-PFP-RX-328 Reactor Building, El 328 0

71111.06 Procedures N2-PRA-012 Nine Mile Point Unit 2 Probabilistic Risk Assessment 3

Internal Flooding Analysis Notebook

71111.11Q Miscellaneous Reactivity October 2021 Quarterly Load Drop 0

Maneuver Plan

NM1C25-3

Reactivity October 2021 Sequence Exchange, Scram Time Testing, 0

Maneuver Plan and Friction Testing

NM2C18-9

Procedures N1-ST-R1 Control Rod Scram Insertion Time Test 02600

N2-OSP-RDS- Channel Interference Testing 00600

@002

71111.12 Corrective Action 01986288

Documents 02005727

02468122

04389154

04412983

04413060

04446429

Corrective Action 04464682

Documents

16

Inspection Type Designation Description or Title Revision or

Procedure Date

Resulting from

Inspection

Miscellaneous (a)(1) Determination Approved

for Unit 2 Service 12/3/21

Water

1-CRAC-F02 Maintenance Rule System Basis Document

Unit 2 Maintenance Automatic Depressurization

Rule System Basis

Document

Unit 2 Maintenance Containment Inerting/N2

Rule System Basis

Document

Unit 2 Maintenance Instrument Air

Rule System Basis

Document

Unit 2 Maintenance Service Water

Rule System Basis

Document

Procedures N1-MMP-210-001 Control Room Chiller Maintenance

Work Orders C91883376

C93774298

C93785657

C93785742

C93786175

71111.13 Procedures OP-AA-108-117 Protected System Verification IAW 7

OP-NM-108-117 Protected Equipment Program at Nine Mile Point 00500

WC-AA-101-1004 On-Line Maintenance For Limiting Condition For Operation 009

of Systems of Components

71111.15 Corrective Action 02715754

Documents 04448532

04449792

04449971

04449971

04453026

17

Inspection Type Designation Description or Title Revision or

Procedure Date

04458203

04459510

Drawings C-18026-C Emergency Diesel Generator #102 Starting Air, Cooling 28

Water Lube Oil and Fuel

C-19410-C Fold Out 10/10A - Elementary Wiring Diagram Diesel 47

Generators #102 and #103 Control Ckts

C-19589-C Elementary Wiring Diagram Reactor Protection System 51

(Emergency Cooling Channel #11)

C-19845-C Elementary Wiring Diagram DC Valve Board 12 26

Procedures N1-ST-M4A Emergency Diesel Generator 102 and PB 102 Operability 03000

Test

N2-OSP-ICS- RCIC Pump and Valve Operability Test and System 01600

Q@002 Integrity Test and ASME XI Functional Test and Analysis

Work Orders C93808212

71111.18 Drawings 0001040209048 Control Diagram Shutdown System 13

PID-104A Piping and Instrumentation Diagram Standby Diesel Gen 34

System

Engineering ECP-21-000437 EDG Governor Booster 0000

Changes

Work Orders C93809772

71111.19 Corrective Action 04380928

Documents 044595101

04461978

Procedures MA-AA-716-012 Post Maintenance Testing 26

N1-EPM-GEN-150 4.16kV Breaker Inspection PM 01800

N1-ST-Q1B CS 121 Pump, Valve and SDC Water Seal Check Valve 02300

Operability Test

N2-MSP-HVK- Control Building Chiller Performance Test 00000

2Y001

N2-OSP-EGS- Diesel Generator and Diesel Air Start Valve Operability 024T1

M@001 Test - Division I and II

N2-OSP-ICS- RCIC Pump and Valve Operability Test and System 01600

Q@002 Integrity Test and ASME XI Functional Test and Analysis

Work Orders C93658634

18

Inspection Type Designation Description or Title Revision or

Procedure Date

C93658635

C93811429

C93812090

C93812875

71111.22 Drawings F-63019-C Reactor Liquid Poison System ASME Section XI Boundary 17

Diagram

Procedures N1-ST-Q4A Liquid Poison Pump 11 and Check Valve Operability Test 01800

N2-ISP-CSL-Q001 LPCS Pump Discharge Flow - Low (Bypass) Instrument 00700

Channel Functional Test

N2-OSP-LOG-S001 Shift Checks - Mode 1 03800

Work Orders C93771647

71151 Corrective Action 04444544

Documents

Miscellaneous N1-MSPI-001 Nine Mile Point 1 MSPI Basis Document 11

N2-MSPI-001 Nine Mile Point 2 MSPI Basis Document 16

NEI 99-02 Regulatory Assessment Performance Indicator Guideline 7

71152 Corrective Action 04289904

Documents 04368005

04371766

04372127

04433486

04439810

04441194

04442220

04446429

04448532

04458203

04459468

4372131

Procedures ER-AA-425 Implementation of Technical Specification Surveillance 004

Frequency Control Program

N1-ISP-036-003 HI/LO Reactor Water Level Instrument Trip Channel 01400

Test/Calibration

19