ML13225A471

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IR 05000220-13-003, 05000410-13-003; on 04/01/2013 - 06/30/2013; Nine Mile Point Nuclear Station (NMPNS) Units 1 and 2; Surveillance Testing, Problem Identification and Resolution, Follow-Up of Events and Notices of Enforcement Discretion
ML13225A471
Person / Time
Site: Nine Mile Point  Constellation icon.png
Issue date: 08/13/2013
From: Daniel Schroeder
Reactor Projects Branch 1
To: Costanzo C
Constellation Energy Nuclear Group
Schroeder D
References
IR-13-003
Download: ML13225A471 (73)


See also: IR 05000220/2013003

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION I

2100 RENAISSANCE BOULEVARD, SUITE 100

KING OF PRUSSIA, PENNSYLVANIA 19406-2713

August 13, 2013

Mr. Christopher Costanzo, Vice President

Nine Mile Point Nuclear Station

Constellation Energy Nuclear Group, LLC

P.O. Box 63

Lycoming, NY 13093

SUBJECT: NINE MILE POINT NUCLEAR STATION - NRC INTEGRATED INSPECTION

REPORT 05000220/2013003 AND 05000410/2013003

Dear Mr. Costanzo:

On June 30, 2013, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at

your Nine Mile Point Nuclear Station (NMPNS) Units 1 and 2. The enclosed inspection report

documents the inspection results, which were discussed on July 25, 2013, with you and other

members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

This report documents one self-revealing apparent violation concerning the improper restoration

of a direct current electrical bus which resulted in a loss of all shutdown cooling. The safety

significance of the violation is still under review pending the outcome of a Phase III risk analysis

by NRC Senior Reactor Analysts. However, the violation does not represent an immediate

safety concern because Constellation has conducted a prompt human performance event

review, entered the issue into their corrective action program (CAP), and conducted a root

cause analysis. Additionally, corrective actions including a review of all emergency, off-normal,

and normal system operating procedures are in progress. This violation with the supporting

circumstances and details is documented in this inspection report.

This report documents two NRC-identified findings and two self-revealing findings of very low

safety significance (Green). These findings were determined to involve violations of NRC

requirements. However, because of the very low safety significance, and because they are

entered into your CAP, the NRC is treating these findings as non-cited violations (NCVs)

consistent with Section 2.3.2 of the NRC Enforcement Policy. If you contest any NCVs in this

report, you should provide a response within 30 days of the date of this inspection report with

the basis of your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control

Desk, Washington D.C. 20555-0001; with copies to the Regional Administrator, Region I; the

Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, D.C.

20555-0001; and the NRC Resident Inspector at NMPNS. In addition, if you disagree with the

C. Costanzo 2

cross-cutting aspect assigned to any finding in this report, you should provide a response within

30 days of the date of this inspection report, with the basis for your disagreement, to the

Regional Administrator, Region I, and the NRC Resident Inspector at NMPNS.

In accordance with Title 10 of the Code of Federal Regulations 2.390 of the NRCs Rules of

Practice, a copy of this letter, its enclosure, and your response (if any) will be available

electronically for public inspection in the NRC Public Document Room or from the Publicly

Available Records component of the NRCs Agencywide Documents Access Management

System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-

rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Daniel L. Schroeder, Chief

Reactor Projects Branch 1

Division of Reactor Projects

Docket Nos: 50-220 and 50-410

License Nos: DPR-63 and NPF-69

Enclosure: Inspection Report 05000220/2013003 and 05000410/2013003

w/Attachment: Supplementary Information

cc w/encl: Distribution via ListServ

ML13225A471

Non-Sensitive Publicly Available

SUNSI Review

Sensitive Non-Publicly Available

OFFICE klm RI/DRP RI/DRP RI/DRP

NAME KKolaczyk/DLS for ARosebrook/DLS for DSchroeder/DLS

DATE 08/13/13 08/13/13 08/13/13

1

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

Docket Nos: 50-220 and 50-410

License Nos: DPR-63 and NPF-69

Report No: 05000220/2013003 and 05000410/2013003

Licensee: Constellation Energy Nuclear Group, LLC (CENG)

Facility: Nine Mile Point Nuclear Station, Units 1 and 2

Location: Oswego, NY

Dates: April 1, 2013 through June 30, 2013

Inspectors: K. Kolaczyk, Senior Resident Inspector

E. Miller, Resident Inspector

B. Dionne, Health Physicist

B. Haagensen, Resident Inspector

P. Kaufman, Senior Reactor Inspector

J. Krafty, Resident Inspector

J. Laughlin, Emergency Preparedness Inspector

J. Lilliendahl, Reactor Inspector

A. Rosebrook, Senior Project Engineer

B. Scrabeck, Project Engineer

Approved by: Daniel L. Schroeder, Chief

Reactor Projects Branch 1

Division of Reactor Projects

Enclosure

2

TABLE OF CONTENTS

SUMMARY.................................................................................................................................... 3

1. REACTOR SAFETY.............................................................................................................. 7

1R01 Adverse Weather Protection ................................................................................... 7

1R04 Equipment Alignment .............................................................................................. 8

1R05 Fire Protection ......................................................................................................... 9

1R07 Heat Sink Performance ........................................................................................... 9

1R08 Inservice Inspection Activities ............................................................................... 10

1R11 Licensed Operator Requalification Program & Licensed Operator Performance .. 12

1R12 Maintenance Effectiveness ................................................................................... 13

1R13 Maintenance Risk Assessments and Emergent Work Control .............................. 13

1R15 Operability Determinations and Functionality Assessments.................................. 14

1R18 Plant Modifications ................................................................................................ 15

1R19 Post-Maintenance Testing ..................................................................................... 15

1R20 Refueling and Other Outage Activities .................................................................. 16

1R22 Surveillance Testing .............................................................................................. 17

1EP4 Emergency Action Level and Emergency Plan Changes ...................................... 20

1EP6 Drill Evaluation ...................................................................................................... 20

2. RADIATION SAFETY.......................................................................................................... 21

2RS1 Radiological Hazard Assessment and Exposure Controls .................................... 21

2RS2 Occupational ALARA Planning and Controls ........................................................ 24

2RS3 In-Plant Airborne Radioactivity Control and Mitigation .......................................... 26

2RS4 Occupational Dose Assessment ........................................................................... 27

2RS7 Radiological Environmental Monitoring Program .................................................. 30

4. OTHER ACTIVITIES ........................................................................................................... 33

4OA1 Performance Indicator Verification ........................................................................ 33

4OA2 Problem Identification and Resolution ................................................................... 33

4OA3 Follow-Up of Events and Notices of Enforcement Discretion ................................ 42

4OA6 Meetings, Including Exit ........................................................................................ 50

ATTACHMENT: SUPPLEMENTARY INFORMATION .............................................................. 50

SUPPLEMENTARY INFORMATION ........................................................................................ A-1

KEY POINTS OF CONTACT .................................................................................................... A-1

LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED ..................................... A-2

LIST OF DOCUMENTS REVIEWED ........................................................................................ A-3

LIST OF ACRONYMS............................................................................................................. A-19

Enclosure

3

SUMMARY

IR 05000220/2013003, 05000410/2013003; 04/01/2013 - 06/30/2013; Nine Mile Point Nuclear

Station (NMPNS) Units 1 and 2; Surveillance Testing, Problem Identification and Resolution,

Follow-Up of Events and Notices of Enforcement Discretion.

This report covered a 3-month period of inspection by resident inspectors and announced

inspections performed by regional inspectors. One apparent violation was identified. The

safety significance of this violation is still under review pending the outcome of a Phase III risk

analysis by NRC Senior Reactor Analysts. Additionally, two NRC-identified findings and two

self-revealing findings of very low safety significance (Green) were identified, all of which were

non-cited violations (NCVs). The significance of most findings is indicated by their color (i.e.,

greater than Green, or Green, White, Yellow, Red) and determined using Inspection Manual

Chapter (IMC) 0609, Significance Determination Process (SDP), dated June 2, 2011. Cross-

cutting aspects are determined using IMC 0310, Components Within the Cross-Cutting Areas,

dated October 28, 2011. All violations of NRC requirements are dispositioned in accordance

with the NRCs Enforcement Policy, dated January 28, 2013. The NRCs program for

overseeing the safe operation of commercial nuclear power reactors is described in NUREG-

1649, Reactor Oversight Process, Revision 4.

Cornerstone: Initiating Events

TBD. A self-revealing apparent violation of Technical Specification (TS) 6.4.1, Procedures,

was identified at Unit 1 because CENG failed to properly recover from a loss of a vital direct

current (DC) bus in accordance with station off-normal procedures resulting in an unplanned

loss of all shutdown cooling (SDC) when time to boil was less than 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />. Specifically,

during the restoration from the loss of battery bus 12, operators failed to identify a SDC trip

signal before attempting restoration of the DC bus, which ultimately lead to a SDC pump trip

(i.e. loss of decay heat removal from the reactor). Corrective actions included conducting a

prompt human performance event review, entering the issue into their corrective action

program (CAP), and conducting a root cause analysis. Planned corrective actions include a

review of all emergency, off-normal, and normal system operating procedures.

The inspectors determined that CENGs failure to properly restore battery bus 12 in

accordance with N1-SOP-47A.1, Loss of DC, Revision 00101, and N1-OP-47A, 125 VDC

Power System, Revision 02500, was a performance deficiency that was reasonably within

CENGs ability to foresee and correct and should have been prevented. The performance

deficiency was determined to be more than minor because the inspectors determined it

affected the configuration control aspect of the Initiating Events cornerstone and adversely

affected the associated cornerstone objective to limit the likelihood of events that upset plant

stability and challenge critical safety functions during shutdown as well as power operations.

The significance of the finding is designated as To Be Determined (TBD) until a Phase 3

analysis can be completed by the NRCs Senior Reactor Analysts. The inspectors

determined this finding has a cross-cutting aspect in the area of Human Performance,

Resources, because CENG did not ensure that personnel, equipment, procedures, and

other resources were available and adequate to assure nuclear safety - complete, accurate

Enclosure

4

and up-to-date design documentation, procedures, work packages, and correct labeling of

components. Specifically, CENG procedures N1-SOP-47A.1 and N1-OP-47A did not

contain adequate guidance to ensure recovery from a loss of a DC bus would not result in

an unexpected plant transient H.2(c). (Section 4OA3)

Cornerstone: Mitigating Systems

Green. A self-revealing NCV of TS 5.4.1, Procedures, was identified at Unit 2 when a

CENG instrumentation and control (I&C) technician did not properly implement procedure

N2-ISP-LDS-Q010, Reactor Building General Area Temperature Instrument Channel

Functional Test, Revision 00102. As a result, a residual heat removal (RHR)/reactor core

isolation cooling (RCIC) isolation bypass switch was inadvertently left in the NORMAL

position during surveillance testing resulting in an unplanned RCIC isolation. CENG entered

this issue into their CAP as CR-2013-002461. Other corrective actions included performing

a human performance stand down that reinforced use of human performance tools and the

need to identify and mark critical steps during pre-job briefs, retraining the I&C technicians

involved in the event on proper use of human performance error prevention techniques, and

improving bypass switch verification steps for procedure N2-ISP-LDS-Q010 and other

similar lead detection system surveillances procedures.

This finding is more than minor because it is associated with the human performance

attribute of the Mitigating Systems cornerstone and affected the cornerstone objective to

ensure the availability, reliability, and capability of systems that respond to initiating events

to prevent undesirable consequences (i.e., core damage). Specifically, the inadvertent

isolation rendered the RCIC system inoperable and unable to perform its function for

approximately 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. Additionally, this finding is similar to example 4.b of IMC 0612,

Appendix E, Examples of Minor issues, and is more than minor due to the procedural error

leading to a plant transient, i.e. an unplanned RCIC isolation. This finding was evaluated in

accordance with IMC 0609.04, Initial Characterization of Findings, and Exhibit 2 of IMC

0609, Appendix A, The Significance Determination Process for Findings At-Power, issued

June 19, 2012. Unit 2 is a boiling-water reactor (BWR)-5, and as a result, RCIC is treated

as having a separate high-pressure injection safety function. A detailed analysis was

conducted using SAPHIRE version 8.0.8.0 and Unit 2 SPAR model 8.17. Using an

exposure period of 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and conservatively assuming no recovery of the failed

equipment, this finding had a change in core damage frequency of low E-8. The dominant

accident sequence was a grid-related loss of offsite power with a failure of Division III power

and the failure to recover offsite power and the emergency diesel generators (EDGs) in 30

minutes. Since the change in core damage frequency was less than 1E-7, contributions

from large early release and external event did not need to be considered. Therefore, this

finding was of very low safety significance (Green). This finding has a cross-cutting aspect

in the area of Human Performance, Work Practices, because the I&C technicians did not

effectively employ self-checking and place-keeping when implementing the test procedure

which directly contributed to the resulting procedural error H.4(a). (Section 1R22)

Green. The inspectors identified an NCV at Unit 2 of Title 10 of the Code of Federal

Regulations (10 CFR) Part 50, Appendix B, Criterion V, Instructions, Procedures, and

Drawings, because CENG did not assure that the replacement of cells in battery 2C were

prescribed and performed by appropriate procedures which resulted in degraded accuracy

Enclosure

5

of test results and potential degradation of safety-related battery cells. In response to this

issue, CENG generated CR-2013-005235 and initiated actions to evaluate replacing the

new cells.

This finding is more than minor because it was associated with the equipment performance

attribute of the Mitigating Systems cornerstone and affected the cornerstone objective to

ensure the availability, reliability, and capability of systems that respond to initiating events

to prevent undesirable consequences. In accordance with IMC 0609.04, Initial

Characterization of Findings, and Exhibit 2 of IMC 0609, Appendix A, The Significance

Determination Process for Findings At-Power, issued June 19, 2012, the inspectors

determined this finding is of very low safety significance (Green) because the performance

deficiency was not a design or qualification deficiency, did not involve an actual loss of

safety function, did not represent actual loss of a safety function of a single train for greater

than its TS allowed outage time, and did not screen as potentially risk-significant due to a

seismic, flooding, or severe weather initiating event. This finding has a cross-cutting aspect

in the area of Human Performance, Decision-Making component, because CENG did not

use conservative assumptions in decision making. Specifically, CENG did not monitor the

cells in storage, question the adequacy of the discharged cells, charge the cells prior to

installation, or fully evaluate the implications of the test and recharge results H.1(b).

(Section 4OA2)

Green. The inspectors identified an NCV at Unit 2 of 10 CFR Part 50, Appendix B,

Criterion III, Design Control, because CENG did not verify the adequacy of the design with

respect to battery 2C. Specifically, by failing to size the battery to the most limiting time

period, the sizing calculation significantly overstated the available design margin. CENGs

corrective actions included generating condition report CR-2013-005117 and evaluating the

condition for operability.

This finding is more than minor because it was associated with the design control attribute of

the Mitigating Systems cornerstone and affected the cornerstone objective to ensure the

availability, reliability, and capability of systems that respond to initiating events to prevent

undesirable consequences. In accordance with IMC 0609.04, Initial Characterization of

Findings, and Exhibit 2 of IMC 0609, Appendix A, The Significance Determination Process

for Findings At-Power, issued June 19, 2012, the inspectors determined this finding is of

very low safety significance (Green) because the performance deficiency was not a design

or qualification deficiency, did not involve an actual loss of safety function, did not represent

actual loss of a safety function of a single train for greater than its TS allowed outage time,

and did not screen as potentially risk-significant due to a seismic, flooding, or severe

weather initiating event. The inspectors did not assign a cross-cutting aspect because the

finding was not indicative of current performance. (Section 4OA2)

Cornerstone: Barrier Integrity

Green. A self-revealing NCV of TS 3.3.3, Leakage Rate, was identified for CENGs failure

from December 3 to December 13, 2012, to maintain containment leakage less than

1.5 percent by weight of the containment air per day and less than 0.6 percent by weight of

the containment air per day for all penetrations and all primary containment isolation valves

subject to 10 CFR Part 50, Appendix J, Types B and C tests, when pressurized to

Enclosure

6

35 pound per square inch gauge when reactor coolant system (RCS) temperature is above

215°F and primary containment integrity is required. CENG entered this issue into their

CAP as CR-2012-011247. Corrective actions included cleaning iron oxide from the primary

containment vent and purge valve and replacing the resilient seals.

This finding is more than minor because it is associated with the structure, system,

component (SSC), and barrier performance attribute of the Barrier Integrity cornerstone and

affected the cornerstone objective to provide reasonable assurance that physical design

barriers (fuel cladding, reactor coolant system, and containment) protect the public from

radionuclide releases caused by accidents or events. Specifically, containment leakage

exceeded the leakage limits outlined in the Unit 1 TS 3.3.3 from December 3 to December

13, 2012. This finding was evaluated in accordance with IMC 0609.04, Initial

Characterization of Findings, and Table 6.2, Phase 2 Risk Significance-Type B Findings at

Full Power, of IMC 0609, Appendix H, Containment Integrity Significance Determination

Process, issued May 6, 2004. The inspectors determined this finding was of very low

safety significance (Green) because the leakage was less than 100 percent of containment

volume per day for the duration of the leak. This finding has a cross-cutting aspect in the

area of Problem Identification and Resolution, CAP, because CENG failed to take

appropriate corrective action to address safety issues and adverse trends in a timely

manner commensurate with their safety significance. Specifically, following identification of

the adverse trend regarding the frequency of nitrogen addition to the drywell, CENG did not

assess in a timely manner the significance of the leakage and the impact on primary plant

containment P.1(d). (Section 4OA3)

Enclosure

7

REPORT DETAILS

Summary of Plant Status

Unit 1 began the inspection period at 100 percent power. On April 14, 2013, Unit 1 reduced

power to 32 percent to conduct emergency condenser testing and to down power for refueling

outage (N1R22). On April 15, Unit 1 was removed from the grid to commence N1R22. Unit 1

returned to service and synchronized to the grid on May 15. On June 21, Unit 1 down powered

to 83 percent to perform a rod pattern adjustment, turbine stop valve replacement, and a reactor

recirculation pump swap. Unit 1 returned to rated power on June 22 and remained at or near

full power for the remainder of the inspection period.

Unit 2 began the inspection period at 100 percent power. On May 28, Unit 2 down powered to

65 percent to investigate diverging feedwater flows between two operating feedwater pumps.

Following identification of a degraded automatic feedwater regulating valve and removal of the

B feedwater pump from service, Unit 2 returned to 100 percent on May 31, and remained at or

near full power for the remainder of the inspection period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection (71111.01 - 2 samples)

.1 Readiness for Seasonal Extreme Weather Conditions

a. Inspection Scope

The inspectors performed a review of CENGs readiness for the onset of seasonal high

temperatures. The review focused on Unit 1 fire protection and diesel fire pump,

technical support center ventilation, control room and reactor building (RB) air

conditioning systems, and Unit 2 service water and heating, ventilation, and air

conditioning systems. The inspectors reviewed the Updated Final Safety Analysis

Report (UFSAR), TSs, and the CAP to determine what temperatures or other seasonal

weather could challenge these systems and to ensure CENG personnel had adequately

prepared for these challenges. The inspectors reviewed station procedures including

CENGs seasonal weather readiness procedure and applicable operating procedures.

The inspectors performed walkdowns of the selected systems to ensure station

personnel identified issues that could challenge the operability of the systems during hot

weather conditions. Documents reviewed for each section of this inspection report are

listed in the Attachment.

b. Findings

No findings were identified.

Enclosure

8

.2 Summer Readiness of Offsite and Alternate Alternating Current (AC) Power Systems

a. Inspection Scope

The inspectors performed a review of plant features and procedures for the operation

and continued availability of the offsite and alternate AC power system to evaluate

readiness of the systems prior to seasonal high grid loading. The inspectors reviewed

changes to CENGs procedures affecting these areas and the communications protocols

between the transmission system operator and CENG implemented since the previous

sample in 2012. This review focused on changes to the established program and

material condition of the offsite and alternate AC power equipment. The inspectors

assessed whether CENG established and implemented appropriate procedures and

protocols to monitor and maintain availability and reliability of both the offsite ac power

system and the onsite alternate AC power system. The inspectors evaluated the material

condition of the associated equipment by interviewing the season readiness coordinator,

reviewing condition reports and open work orders and walking down portions of the

offsite and AC power systems including the 345 kilovolt (kV) and 115 kV switchyards.

b. Findings

No findings were identified.

1R04 Equipment Alignment

Partial System Walkdown (71111.04Q - 5 samples)

a. Inspection Scope

The inspectors performed partial walkdowns of the following systems:

Unit 1, Spent fuel pool (SFP) cooling system during the conduct of refueling

maintenance related activities on April 15, 2013

Unit 1, Core sprays 112 and 122 following the completion of surveillance activities on

April 21, 2013

Unit 1, Isolation condenser loop 12 following the completion of maintenance activities

on May 15, 2013

Unit 1, Diesel and electric fire pumps while the maintenance fire pump was operating

with a degraded discharge relief valve on May 22, 2013

Unit 1, Control room emergency ventilation system following the completion of

maintenance activities on May 30, 2013

The inspectors selected these systems based on their risk-significance relative to the

reactor safety cornerstones at the time they were inspected. The inspectors reviewed

applicable operating procedures, system diagrams, the UFSAR, TSs, work orders,

condition reports, and the impact of ongoing work activities on redundant trains of

equipment in order to identify conditions that could have impacted system performance

of their intended safety functions. The inspectors also performed field walkdowns of

accessible portions of the systems to verify system components and support equipment

were aligned correctly and were operable. The inspectors examined the material

condition of the components and observed operating parameters of equipment to verify

Enclosure

9

that there were no deficiencies. The inspectors also reviewed whether CENG staff had

properly identified equipment issues and entered them into the CAP for resolution with

the appropriate significance characterization.

b. Findings

No findings were identified.

1R05 Fire Protection

Resident Inspector Quarterly Walkdowns (71111.05Q - 6 samples)

a. Inspection Scope

The inspectors conducted tours of the areas listed below to assess the material

condition and operational status of fire protection features. The inspectors verified that

CENG controlled combustible materials and ignition sources in accordance with

administrative procedures. The inspectors verified that fire protection and suppression

equipment was available for use as specified in the area pre-fire plan, and passive fire

barriers were maintained in good material condition. The inspectors also verified that

station personnel implemented compensatory measures for out of service, degraded, or

inoperable fire protection equipment, as applicable, in accordance with procedures.

Unit 1, Drywell (FA3/R1) on April 16, 2013

Unit 1, RB elevation 340 feet (FA1/R6A and FA2/R6B) on April 19, 2013

Unit 1, RB elevation 198 feet southwest (FA2/R1B) on April 21, 2013

Unit 1, RB elevation 237 feet east (FA1/R1A) on April 21, 2013

Unit 1, RB elevation 237 feet west (FA2/R1B) on April 21, 2013

Unit 1, Power board 12 (FA-17A) on April 26, 2013

b. Findings

No findings were identified.

1R07 Heat Sink Performance (71111.07 - 2 samples)

a. Inspection Scope

The inspectors reviewed the samples listed below to determine their readiness and

availability to perform their safety functions. The inspectors reviewed the design basis

for the components and verified CENGs commitments to NRC Generic Letter 89-13.

The inspectors discussed the results of the most recent inspection with engineering staff

and reviewed pictures of the as-found and as-left conditions. The inspectors verified that

CENG initiated appropriate corrective actions for identified deficiencies.

Unit 1, Emergency diesel generator (EDG) 103 raw water heat exchanger on

May 3, 2013

Unit 2, 2HVY*UC2A service water pump bay A unit cooler on May 7, 2013

Enclosure

10

1R08 Inservice Inspection Activities (71111.08 - 1 sample)

a. Inspection Scope

From April 15 to 18, 2013, the inspectors conducted a review of CENGs implementation

of inservice inspection (ISI) program activities for monitoring degradation of the RCS

boundary and risk-significant piping system boundaries for Unit 1 during the N1R22.

The sample selection was based on the inspection procedure objectives and risk priority

of those components and systems where degradation would result in a significant

increase in risk of core damage. The inspectors observed in-process nondestructive

examinations (NDEs), reviewed documentation, and interviewed CENG personnel to

verify that the NDE activities performed were conducted in accordance with the

requirements of the American Society of Mechanical Engineers (ASME) Boiler and

Pressure Vessel Code,Section XI, 2004 Edition.

NDE Activities and Welding Activities

The inspectors performed direct observations of NDE activities in process and reviewed

records of NDEs listed below:

ASME Code Required Examinations

Remote visual examination (VT-3) of reactor vessel nozzle N16-1-N3A and manual

ultrasonic testing (UT) examination of three 12-inch diameter emergency condenser

supply piping welds.

Data records of manual UT phased array examination of five 28-inch diameter

reactor vessel nozzle-to-vessel dissimilar metal safe end-to-nozzle welds (32-WD-

042, N2A; 32-WD-082, N2B; 32-WD-122, N2C; 32-WD-164, N2D; 32-WD-208, N2E),

manual UT of four 12-inch diameter emergency condenser supply piping welds, dye

penetrant testing and UT of branch connection-decontamination port welds on the

recirculation system suction piping, and UT thickness readings of various diameter

RB closed loop cooling system piping located at elevation 225 foot in the drywell.

The inspectors reviewed certifications of the NDE technician, process, and equipment in

identifying the condition or degradation of risk-significant SSCs and evaluated the

activities for compliance with the requirements of Unit 1s risk informed ISI program,

ASME Boiler and Pressure Vessel Code,Section XI, and 10 CFR 50.55a.

Augmented or Industry Imitative Examinations

Based on industry operating experience, the inspectors reviewed NDE data records of

the recirculation system suction piping decontamination port branch connection welds to

verify that the activities were performed in accordance with applicable examination

procedures and industry guidance.

Modification/Repair/Replacement Consisting of Welding Activities

The inspectors reviewed the following welding activities to verify specifications and

control of the welding processes, weld procedures, welder qualifications, and NDE

examinations were in accordance with ASME code requirements.

Enclosure

11

The repair and replacement of reactor water cleanup (RWCU) dissimilar metal pipe weld

33-WD-046 was reviewed. The inspectors reviewed the associated flaw evaluation,

NDE data records, and repair/replacement WO package.

During manual phased array UT of a 6-inch diameter schedule 80 stainless steel pipe to

carbon steel RWCU pipe dissimilar metal weld, a 4.25-inch long circumferential flaw

indication was detected in the heat-affected zone of the stainless steel side of the weld.

The indication did not meet ASME Code,Section XI 2004, IWB-3514-2 acceptance

criteria so a flaw evaluation was required. The flaw evaluation concluded that sufficient

structural margin was demonstrated for the as-found flaw indication.

However, a review of construction radiographs by CENG indicated that there had been

two previous weld repairs directly adjacent to this indication. CENG determined that the

residual stresses of the weld were likely to be high due to the prior weld repairs and the

crack growth rate would be high enough to possibly propagate the flaw beyond the

ASME code limit of through-thickness. Based on this information, CENG replaced the

weld and adjacent pipe by installing a new spool piece.

The inspectors verified the welding activities and applicable NDE techniques were

performed in accordance with ASME Code requirements.

Re-examination of an Indication Previously Accepted for Service After Analysis

There were no samples available for review during this inspection that involved

examinations with recordable indications that have been accepted for continued service

from the previous Unit 1 outage through the current outage.

Drywell Visual Examination

The inspectors examined the condition of Unit 1 drywell liner surface at various elevation

levels inside the drywell. During the inspection, surface corrosion was noted on the

drywell liner and on several systems including the RB closed-cooling water system.

CENG was monitoring the condition of the liner and RB closed-cooling water system to

ensure the corrosion was not impacting system or component operability.

Identification and Resolution of Problems

The inspectors reviewed a sample of condition reports which involved ISI-related

activities to confirm that non-conformances were being properly identified, reported, and

resolved.

b. Findings

No findings were identified.

Enclosure

12

1R11 Licensed Operator Requalification Program and Licensed Operator Performance

(71111.11Q - 4 samples)

.1 Quarterly Review of Licensed Operator Requalification Testing and Training (2 samples)

a. Inspection Scope

The inspectors observed:

Unit 1, Licensed operator simulator training which included a loss of condenser

vacuum, a stuck open electro-matic relief valve (ERV), and an anticipated transient

without scram on April 2, 2013

Unit 2, Licensed operator performance during a simulator training scenario that

included high temperatures on the main transformer, degraded service water, and a

loss of the offsite electrical grid on May 23, 2013

The inspectors evaluated operator performance during the simulated event and verified

completion of risk-significant operator actions, including the use of abnormal and

emergency operating procedures. The inspectors assessed the clarity and effectiveness

of communications, implementation of actions in response to alarms and degrading plant

conditions, and the oversight and direction provided by the control room supervisor. The

inspectors verified the accuracy and timeliness of the emergency classifications made by

the shift manager and the TS action statements entered by the shift technical advisor.

Additionally, the inspectors assessed the ability of the crew and training staff to identify

and document crew performance problems.

b. Findings

No findings were identified.

.2 Quarterly Review of Licensed Operator Performance in the Main Control Room

(2 samples)

a. Inspection Scope

The inspectors observed:

Unit 2, Control room operations during a period of increased site activity due to a

failure of an on-site power loop that supplied electrical power to several non-

essential buildings within the protected area as well as several plant information

technology systems on April 9, 2013

Unit 1, Control room operations during a plant shutdown to commence planned

refueling outage N1R22 on April 14, 2013

The inspectors reviewed CNG-OP-1.01-1000, Conduct of Operations, Revision 00900,

and verified that procedure use, crew communications, and coordination of plant

activities among work groups similarly met established expectations and standards.

Additionally, the inspectors observed test performance to verify that procedure use, crew

communications, and coordination of activities between work groups similarly met

established expectations and standards.

Enclosure

13

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness (71111.12Q - 4 samples)

a. Inspection Scope

The inspectors reviewed the samples listed below to assess the effectiveness of

maintenance activities on SSC performance and reliability. The inspectors reviewed

system health reports, CAP documents, maintenance work orders, and maintenance

rule basis documents to ensure that CENG was identifying and properly evaluating

performance problems within the scope of the maintenance rule. For each sample

selected, the inspectors verified that the SSC was properly scoped into the maintenance

rule in accordance with 10 CFR 50.65 and verified that the (a)(2) performance criteria

established by CENG staff was reasonable. As applicable, for SSCs classified as (a)(1),

the inspectors assessed the adequacy of goals and corrective actions to return these

SSCs to (a)(2). Additionally, the inspectors ensured that CENG staff was identifying and

addressing common cause failures that occurred within and across maintenance rule

system boundaries.

Unit 1, Neutron monitoring on May 14, 2013

Unit 2, High-pressure core spray (HPCS) on May 14, 2013

Unit 1, Service water on May 16, 2013

Unit 1, Containment spray on May 17, 2013

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13 - 8 samples)

a. Inspection Scope

The inspectors reviewed station evaluation and management of plant risk for the

maintenance and emergent work activities listed below to verify that CENG performed

the appropriate risk assessments prior to removing equipment from service. The

inspectors selected these activities based on potential risk significance relative to the

reactor safety cornerstones. As applicable for each activity, the inspectors verified that

CENG personnel performed risk assessments as required by 10 CFR 50.65(a)(4) and

that the assessments were accurate and complete. When CENG performed emergent

work, the inspectors verified that operations personnel promptly assessed and managed

plant risk. The inspectors reviewed the scope of maintenance work and discussed the

results of the assessment with the stations probabilistic risk analyst to verify plant

conditions were consistent with the risk assessment. The inspectors also reviewed the

TS requirements and inspected portions of redundant safety systems, when applicable,

to verify risk analysis assumptions were valid and applicable requirements were met.

Enclosure

14

Unit 2, Unplanned elevated risk condition that resulted from an inadvertent isolation

of the RCIC system on April 2, 2013

Unit 2, Loss of maintenance supply power to 2VBB*UPS3B on April 5, 2013

Unit 1, Power boards 102 and 16 following electrical realignment on May 1, 2013

Unit 1, Planned maintenance on pressure safety valve 201.970, emergency

condenser vent isolation IV-05-03, and emergency condenser 112 HX HTX-60-44 on

May 2, 2013

Unit 2, Planned maintenance on the Division I control room air conditioning system

on May 13, 2013

Unit 1, Unplanned maintenance on the turbine bypass valve control system on

May 14, 2013

Unit 1, Planned maintenance on the 102 EDG raw water pump on May 23, 2013

Unit 2, Unplanned maintenance on the 2SWP*P1B service water pump on June 11,

2013

b. Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessments (71111.15 - 9 samples)

a. Inspection Scope

The inspectors reviewed operability determinations for the following degraded or non-

conforming conditions:

Unit 1, Acceptance criteria associated with N1-ST-C5, secondary containment, and

RB emergency ventilation system operability testing on April 13, 2013

Unit 1, Emergency service water 11 pump (72-04) trip during surveillance testing on

April 17, 2013

Unit 1, Damaged containment spray nozzle deflectors on May 3, 2013

Unit 1, Source range monitors due to under-vessel work on May 3, 2013

Unit 1, Steam leakage from vent valve 05-11 on May 19, 2013

Unit 2, RCIC high-energy line break barrier door on May 20, 2013

Unit 1, Core spray topping pump 122 bearing cooling water flow on June 11, 2013

Unit 2, Elevated drywell floor drain leakage on June 11, 2013

Unit 1, Elevated drywell floor drain leakage on June 25, 2013

The inspectors selected these issues based on the risk significance of the associated

components and systems. The inspectors evaluated the technical adequacy of the

operability determinations to assess whether TS operability was properly justified and

the subject component or system remained available such that no unrecognized

increase in risk occurred. The inspectors compared the operability and design criteria in

the appropriate sections of the TSs and UFSAR to CENGs evaluations to determine

whether the components or systems were operable. Where compensatory measures

were required to maintain operability, the inspectors determined whether the measures

in place would function as intended and were properly controlled by CENG. The

inspectors determined, where appropriate, compliance with bounding limitations

associated with the evaluations.

Enclosure

15

b. Findings

No findings were identified.

1R18 Plant Modifications (71111.18 - 3 samples)

.1 Temporary Modifications (1 sample)

a. Inspection Scope

The inspectors reviewed a temporary change to ventilation damper 2HVP*AOD5A which

supplies outside air to the Division III diesel generator room. The inspectors reviewed

10 CFR 50.59 documentation and conducted a field walkdown of the modification to

verify that the temporary modification did not degrade the design bases, licensing bases,

and performance capability of the affected systems.

b. Findings

No findings were identified.

.2 Permanent Modifications (2 samples)

a. Inspection Scope

The inspectors evaluated the following modifications:

Engineering Change Package (ECP) 12-00616 - Installation of a damper for Unit 1

downstream of BV-210-25

ECP 13-000167 - Installation of replacement pump for Unit 1 service water radiation

monitor

The inspectors verified that the design bases, licensing bases, and performance

capability of the affected system was not degraded by the modifications. In addition, the

inspectors reviewed modification documents associated with the upgrade and design

change including the post-installation test procedure, the 10 CFR 50.59 screening form,

and the operational impact assessment form.

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing (71111.19 - 5 samples)

a. Inspection Scope

The inspectors reviewed the post-maintenance tests for the maintenance activities listed

below to verify that procedures and test activities ensured system operability and

functional capability. The inspectors reviewed the test procedure to verify that the

procedure adequately tested the safety functions that may have been affected by the

maintenance activity, that the acceptance criteria in the procedure was consistent with

Enclosure

16

the information in the applicable licensing basis and/or design basis documents, and that

the procedure had been properly reviewed and approved. The inspectors also

witnessed the test or reviewed test data to verify that the test results adequately

demonstrated restoration of the affected safety functions.

Unit 1, Control room ventilation/smoke purge system test following installation of fire

damper BV-21-036 on April 3, 2013

Unit 1, Power board 102 following National Fire Protection Act 805 modification on

April 28, 2013

Unit 1, Isolation valve IV-39-10R following control circuit stop relay replacement on

May 9, 2013

Unit 1, Replacement of excess flow check valve CKV-32-138 on May 10, 2013

Unit 1, IV-29-07R diagnostic testing following body-to-bonnet seal replacement on

May 23, 2013

b. Findings

No findings were identified.

1R20 Refueling and Other Outage Activities (71111.20 - 1 sample)

a. Inspection Scope

The inspectors reviewed the stations work schedule and outage risk plan for the Unit 1

maintenance and refueling outage (N1R22) which was conducted April 14 through May

15, 2013. The inspectors reviewed CENGs development and implementation of outage

plans and schedules to verify that risk, industry experience, previous site-specific

problems, and defense-in-depth were considered. During the outage, the inspectors

observed portions of the shutdown and cooldown processes and monitored controls

associated with the following outage activities:

Configuration management, including maintenance of defense-in-depth,

commensurate with the outage plan for the key safety functions and compliance with

the applicable TSs when taking equipment out of service

Implementation of clearance activities and confirmation that tags were properly hung

and that equipment was appropriately configured to safely support the associated

work or testing

Installation and configuration of reactor coolant pressure, level, and temperature

instruments to provide accurate indication and instrument error accounting

Status and configuration of electrical systems and switchyard activities to ensure that

TSs were met

Monitoring of decay heat removal operations

Impact of outage work on the ability of the operators to operate the SFP cooling

system

Reactor water inventory controls, including flow paths, configurations, alternative

means for inventory additions, and controls to prevent inventory loss

Activities that could affect reactivity

Maintenance of secondary containment as required by TSs

Refueling activities

Fatigue management

Enclosure

17

Tracking of startup prerequisites, walkdown of the drywell (primary containment) to

verify that debris had not been left which could block the emergency core cooling

system suction strainers, and startup and ascension to full power

Identification and resolution of problems related to refueling activities

b. Findings

No findings were identified.

1R22 Surveillance Testing (71111.22 - 8 samples)

a. Inspection Scope

The inspectors observed performance of surveillance tests and/or reviewed test data of

selected risk-significant SSCs to assess whether test results satisfied TSs, the UFSAR,

and CENG procedure requirements. The inspectors verified that test acceptance criteria

were clear, tests demonstrated operational readiness and were consistent with design

documentation, test instrumentation had current calibrations and the range and accuracy

for the application, tests were performed as written, and applicable test prerequisites

were satisfied. Upon test completion, the inspectors considered whether the test results

supported that equipment was capable of performing the required safety functions. The

inspectors reviewed the following surveillance tests:

N1-ST-Q3, Unit 1, High-Pressure Coolant Injection Pump and Check Valve

Operability Test for Train 12 on April 1, 2013

N1-ST-C5, Unit 1, Secondary Containment and Reactor Building Emergency

Ventilation System Operability Test for Loop 11 on April 8, 2013

N1-ISP-LRT-TYC, Unit 1, Local Leak Rate Test for Valves IV-201-09 and IV-201-10

on April 9, 2013

N2-ISP-LDS-Q010, Unit 2, Reactor Building General Area Temperature Instrument

Channel Functional Test on April 18, 2013

Unit 2, RCS Leakage Determination Surveillance and Calculations on April 24, 2013

N2-CSP-GEN-D100, Unit 2, Reactor Water/Auxiliary Water Chemistry Surveillance

on April 24, 2013

N1-TSP-201-001, Unit 1, Integrated Leak Rate Test of Primary Containment Type A

Test on May 8, 2013

N1-ST-Q15, Unit 1, Condensate Transfer System Operability Test on May 30, 2013

b. Findings

Introduction. A self-revealing Green NCV of TS 5.4.1, Procedures, was identified at

Unit 2 when a CENG I&C technician did not properly implement procedure N2-ISP-LDS-

Q010, Reactor Building General Area Temperature Instrument Channel Functional

Test, Revision 00102. As a result, a RHR/RCIC isolation bypass switch was

inadvertently left in the NORMAL position during surveillance testing resulting in an

unplanned RCIC isolation.

Description. The RCIC system is designed to provide adequate makeup water to the

reactor pressure vessel (RPV) automatically or manually following an RPV isolation

accompanied by a loss of coolant flow from the feedwater system. In the event the

Enclosure

18

steam piping to the RCIC pump system leaks, temperature sensors in the RCIC pump

room will close isolation valves in the RCIC system stopping the leak. CENG

surveillance procedure N2-ISP-LDS-Q010 is a TS surveillance test that verifies that the

group 5 (RHR) and group 10 (RCIC) isolation trip signals will close the respective

system isolation valves if a high-temperature condition occurs. The procedure tests this

function by simulating a high temperature condition and verifying correct system

response. Actual valve movement during testing is prevented by control room operators

blocking the test signal.

On April 2, 2013, an unplanned RCIC isolation occurred when I&C technicians did not

properly implement procedure N2-ISP-LDS-Q010 to block the test signal. Specifically,

step 7.2.1 required I&C technicians to request control room operators to place channel

bypass switch E31A-S4B RHR/RCIC ISOLATION BYPASS in BYPASS and to verify the

circuit was bypassed by observing annunciator and plant computer alarms prior to lifting

thermocouple leads in the field. This was not accomplished which resulted in the

isolation of the RCIC system.

Prior to the event, a pre-job brief was conducted by CENG I&C technicians performing

the work which focused on the roles and responsibilities of personnel including the lifting

of thermocouple leads safely and error free. Placing the RHR/RCIC isolation bypass

switch in BYPASS was not identified as a critical step, and no critical steps were

annotated in the work document as required by CNG-PR-1.01-1009, Procedure and

Work Order Use and Adherence Requirements, Revision 00701. However, the

requirement for operations personnel to place the isolation switch in BYPASS was

discussed during the procedure review with the control room supervisor who assigned a

control room operator to perform the task when requested by I&C technicians. Section

3.12 of CNG-PR-1.01-1009 defines place-keeping as physically marking steps to

prevent the omission or duplication of the steps to maintain an accounting of steps in

progress, steps completed, steps not applicable, and steps not yet performed. It lists

among high-risk practices to be avoided by signing or checking off a step as completed

before it is completed. After commencing surveillance procedure N2-ISP-LDS-Q010,

technicians used improper self-checking and place-keeping by checking and initialing as

complete step 7.2.1 to request operators to place the RHR/RCIC isolation bypass switch

in BYPASS and to verify annunciator and computer alarm points were in alarm without

that step having been performed. Consequently, when thermocouple leads were lifted in

the following step, a false high-temperature signal was generated resulting in the closing

of RCIC steam supply isolation valves 2ICS*MOV121, 2ICS*MOV128, 2ICS*MOV170,

and an unplanned isolation of RCIC. The surveillance test was immediately stopped, the

required TS action statements were entered for the RCIC system, and the system was

restored to an operable status after approximately 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. The isolation signal was also

sent to the RHR system for SDC supply and return valves and for reactor head spray

isolation valve which were already closed at power. There was no impact on operability

of low-pressure coolant injection or containment spray functions of RHR.

A CENG investigation concluded human error as the primary cause for the inadvertent

isolation of the RCIC system. A contributing cause was the failure to implement

adequate corrective actions following a similar RCIC isolation event in 2007. Immediate

corrective actions for this event included a human performance stand down that

reinforced use of human performance tools and the need to identify and mark critical

steps during pre-job briefs, retraining the I&C technicians involved in the event on proper

use of human performance error prevention techniques, and improving bypass switch

Enclosure

19

verification steps for procedure N2-ISP-LDS-Q010 and other similar leak detection

system surveillance procedures. CENG entered this issue in their CAP as CR-2013-

002461.

Analysis. The inspectors determined that CENGs failure to correctly implement

surveillance test procedure N2-ISP-LDS-Q010 was a performance deficiency that was

within CENGs ability to foresee and correct and should have been prevented. This

finding is more than minor because it is associated with the human performance attribute

of the Mitigating Systems cornerstone and affected the cornerstone objective to ensure

the availability, reliability, and capability of systems that respond to initiating events to

prevent undesirable consequences (i.e., core damage). Specifically, the inadvertent

isolation rendered the RCIC system inoperable and unable to perform its function for

approximately 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. Additionally, this finding is similar to Example 4.b. of IMC 0612,

Appendix E, Examples of Minor Issues, and is more than minor due to the procedural

error leading to a plant transient, i.e. an unplanned RCIC isolation.

In accordance with IMC 0609.04, Initial Characterization of Findings, and Exhibit 2 of

IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power,

issued June 19, 2012, this finding represents a loss of safety function. Unit 2 is a

BWR-5, and as a result, RCIC is treated as having a separate high- pressure injection

safety function. A detailed analysis was conducted using SAPHIRE Version 8.0.8.0 and

Unit 2 SPAR Model 8.17. Using an exposure period of 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and conservatively

assuming no recovery of the failed equipment, this finding had a change in core damage

frequency of low E-8. The dominant accident sequence was a grid- related loss of off-

site power with a failure of Division III power and the failure to recover off-site power and

the EDGs in 30 minutes. Since the change in core damage frequency was less than

1E-7, contributions from large early release and external event did not need to be

considered. Therefore, this finding was determined to be of very low safety significance

(Green).

This finding had a cross-cutting aspect in the area of Human Performance, Work

Practices, because the I&C technicians did not effectively employ self-checking and

place-keeping when implementing N2-ISP-LDS-Q010 which directly contributed to the

resulting procedural error H.4(a).

Enforcement. TS 5.4.1, Procedures, requires written procedures to be established,

implemented, and maintained covering the applicable procedures recommended in

Regulatory Guide (RG) 1.33, Quality Assurance Program Requirements (Operation),

Appendix A, Revision 2, dated February 1978. Section 8.b(2)(b) of RG 1.33 requires, in

part, specific procedures for surveillance tests on containment isolation. CENG

surveillance test procedure N2-ISP-LDS-Q010, Reactor Building General Area

Temperature Instrument Channel Functional Test, directed that the RHR/RCIC

ISOLATION BYPASS switch be placed in BYPASS to prevent an inadvertent

containment isolation while lifting thermocouple leads. Contrary to above, on April 2,

2013, technicians lifted thermocouple leads without ensuring the isolation switch was

bypassed, resulting in an unplanned isolation of the RCIC system. Because this issue is

of very low safety significance (Green) and was entered into CENGs CAP as CR-2013-

002461, this violation is being treated as an NCV, consistent with Section 2.3.2 of the

NRC Enforcement Policy. (NCV 05000410/2013003-01, Failure to Follow

Containment Isolation System Surveillance Procedure Resulting in Isolation of the

Reactor Coolant Isolation Cooling System)

Enclosure

20

Cornerstone: Emergency Preparedness

1EP4 Emergency Action Level and Emergency Plan Changes (71114.04 - 1 sample)

a. Inspection Scope

The Office of Nuclear Security and Incident Response headquarters staff performed an

in-office review of the latest revisions of various emergency plan implementing

procedures and the emergency plan located under ADAMS accession number

ML131071146 as listed in the Attachment.

CENG determined that in accordance with 10 CFR 50.54(q), the changes made in the

revisions resulted in no reduction in the effectiveness of the plan and that the revised

plan continued to meet the requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR

Part 50. The NRC review was not documented in a safety evaluation report and did not

constitute approval of CENG-generated changes; therefore, this revision is subject to

future inspection.

b. Findings

No findings were identified.

1EP6 Drill Evaluation (71114.06 - 1 sample)

Training Observation

a. Inspection Scope

The inspectors observed a simulator training evolution for CENGs licensed operators on

April 2, 2013, which required emergency plan implementation by an operations crew.

The inspectors observed Unit 1 licensed operator performance during an evaluated

simulator scenario that included a loss of condenser vacuum, a stuck open ERV, and an

anticipated transient without scram. CENG planned for this evolution to be evaluated

and included in performance indicator data regarding drill and exercise performance.

The inspectors observed event classification and notification activities performed by the

crew. The focus of the inspectors activities was to note any weaknesses and

deficiencies in the crews performance and ensure that CENG evaluators noted the

same issues and entered them into the CAP.

b. Findings

No findings were identified.

Enclosure

21

2. RADIATION SAFETY

Cornerstone: Public Radiation Safety and Occupational Radiation Safety

2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01)

a. Inspection Scope

From April 22 to 25, 2013, the inspectors reviewed and assessed CENGs performance

in assessing the radiological hazards and exposure control in the workplace associated

with licensed activities and the implementation of appropriate monitoring and exposure

control measures for both individual and collective exposures.

The inspectors interviewed the radiation protection manager, radiation protection

supervisors, radiation protection technicians (RPTs), and radiation workers. The

inspectors performed walkdowns of various portions of the plant, performed independent

radiation dose rate measurements, observed work activities in radiological control areas,

and reviewed CENG documents during the N1R22 outage. The inspectors used the

requirements in 10 CFR 20, guidance in Regulatory Guide (RG) 8.38, Control of Access

to High and Very High Radiation Areas of Nuclear Plants, TSs, and CENGs procedures

required by TSs as criteria for determining compliance.

Inspection Planning

The inspectors reviewed the results of radiation protection program audits. The

inspectors reviewed reports of operational occurrences related to occupational radiation

safety since the last inspection on March 21, 2013.

Radiological Hazard Assessment

The inspectors conducted walkdowns and independent radiation measurements to

evaluate material, work and radiological conditions in the facility including the drywell,

RB, refueling floor, and turbine building (TB).

The inspectors selected the following radiological risk-significant work activities that

involved exposure to radiation:

Refueling floor activities

Drywell control rod drive under-vessel work

Drywell scaffolding

Drywell ISI

RWCU valve repairs

For these work activities, the inspectors assessed whether the pre-work surveys

performed were appropriate to identify and quantify the radiological hazard and to

establish adequate protective measures. The inspectors evaluated the radiological

survey program to determine if radiological hazards were properly identified.

The inspectors observed work in potential airborne radioactivity areas and evaluated

whether the air samples from under the reactor vessel, from the reactor cavity and for

Enclosure

22

entries into the tent for repair of the SFP gate, were representative of the breathing air

zone and were properly evaluated. The inspectors evaluated whether continuous air

monitors on the refueling floor in the RB and at the drywell entrance were located to

ensure appropriate detection sensitivity and were representative of actual work areas.

The inspectors evaluated CENGs program for monitoring levels of loose surface

contamination in areas of the plant.

Instructions to Workers

The inspectors reviewed the following radiation work permits (RWPs) used to access

high radiation areas and evaluated if the specified work control instructions and control

barriers were consistent with TS requirements for locked high radiation areas:

RWP 113330H, RB 261 RWCU Valve Work

RWP 113802H, Drywell Under-Vessel Work

RWP 113890A, RB 340 Reactor Disassembly and Reassembly

RWP 113890B, RB 340 Underwater Work on Refuel Floor

RWP 113890E, RB 340 Reactor Cavity and Equipment Storage Pit Decon

RWP 113806H, Drywell ISI

RWP 113815, RB 261 Flow Accelerated Corrosion (FAC) ISI

RWP 113810, Drywell General Scaffolding Activities

The inspectors assessed whether permissible dose for radiological-significant work

under each RWP was clearly identified. The inspectors evaluated whether electronic

personal dosimeter alarm set points were in conformance with survey indications and

plant procedural requirements.

The inspectors reviewed CR-2013-002474 and CR-2012-002974 for occurrences where

a workers electronic personal dosimeter noticeably malfunctioned or alarmed. The

inspectors evaluated whether workers responded appropriately to the off-normal

condition. The inspectors assessed whether the issue was included in the CAP and

whether compensatory dose evaluations were conducted.

For work activities that could suddenly and severely increase radiological conditions, i.e.,

upper elevation of drywell during spent fuel movement and low power range monitor

moves, the inspectors assessed CENGs means to inform workers of these changes that

could significantly impact their occupational dose.

Contamination and Radioactive Material Control

The inspectors observed the access control point where CENG monitors potentially

contaminated material leaving the radiological control area and inspected the methods

used for control, survey, and release from these areas. The inspectors observed the

performance of personnel surveying and releasing material for unrestricted use and

evaluated whether the release surveys were performed in accordance with plant

procedures and process knowledge concerning the equipment.

Enclosure

23

Radiological Hazards Control and Work Coverage

The inspectors evaluated ambient radiological conditions and performed independent

radiation measurements during plant walkdowns. The inspectors assessed whether the

conditions were consistent with applicable posted surveys, RWPs, and associated

worker briefings.

The inspectors assessed whether radiation monitoring devices were placed on the

individuals body consistent with CENG procedures. The inspectors assessed whether

the dosimeter was placed in the location of highest expected dose and that CENG

properly implemented an NRC-approved method of determining effective dose

equivalent.

The inspectors reviewed the application of dosimetry to effectively monitor exposure to

personnel in high radiation work areas with significant dose rate gradients; e.g., RWCU

repairs and workers under vessel in the control rod drive area.

The inspectors reviewed the following RWPs for work within airborne radioactivity areas

with the potential for individual worker internal exposures:

RWP 113802H, Under-Vessel Control Rod Drive Work

RWP 113330H, RWCU Valve Work

RWP 113890E, RB 340 Reactor Cavity and Equipment Storage Pit Decontamination

The inspectors evaluated airborne radioactive controls and monitoring including potential

for significant airborne levels. The inspectors assessed applicable containment barriers

integrity and the operation of temporary high-efficiency particulate air ventilation system.

Risk-Significant High Radiation Area and Very High Radiation Area Controls

The inspectors discussed the controls and procedures for high risk high radiation areas

and very high radiation areas with the radiation protection manager. The inspectors

discussed with first-line health physics supervisors the controls in place for special areas

that have the potential to become very high radiation areas during refueling outages.

The inspectors evaluated the controls for very high radiation areas and areas with the

potential to become a very high radiation area to ensure that an individual was not able

to gain unauthorized access to these areas.

Radiation Worker Performance

The inspectors observed the performance of radiation workers during the N1R22 with

respect to stated radiation protection work requirements. The inspectors assessed

whether workers were aware of the radiological conditions in their workplace, the RWP

controls and limits, and whether their behavior reflected the level of radiological hazards

present.

Radiation Protection Technician Proficiency

The inspectors observed the performance of the RPTs during the N1R22 with respect to

controlling radiation work. The inspectors evaluated whether technicians were aware of

Enclosure

24

the radiological conditions in their workplace, the RWP controls and limits, and whether

their behavior was consistent with their training and qualifications with respect to the

radiological hazards and work activities.

Problem Identification and Resolution

The inspectors evaluated whether problems associated with radiation monitoring and

exposure control were being identified by CENG at an appropriate threshold and were

properly addressed for resolution in the CENGs CAP. The inspectors assessed the

appropriateness of the corrective actions for a selected sample of problems documented

by CENG that involved radiation monitoring and exposure controls. The inspectors

assessed CENGs process for applying operating experience to their plant.

b. Findings

No findings were identified.

2RS2 Occupational ALARA Planning and Controls (71124.02)

a. Inspection Scope

The inspectors assessed performance with respect to maintaining occupational

individual and collective radiation exposures as low as reasonably achievable (ALARA)

during the N1R22. The inspectors used the requirements in 10 CFR 20, RG 8.8,

Information Relevant to Ensuring that Occupational Radiation Exposures at Nuclear

Power Stations will be As Low As Is Reasonably Achievable, RG 8.10, Operating

Philosophy for Maintaining Occupational Radiation Exposures As Low As Is Reasonably

Achievable, TSs, and CENGs procedures required by TSs as criteria for determining

compliance.

Inspection Planning

The inspectors reviewed pertinent information regarding CENGs collective dose history,

current exposure trends, and ongoing or planned activities in order to assess current

performance and exposure challenges.

The inspectors reviewed changes in the radioactive source term by reviewing the trend

in average contact dose rates on reactor recirculation piping for the time period between

1984 and the present Unit 1 outage. The inspectors reviewed ALARA procedures that

specified the processes used to estimate and track exposures for radiological work

activities.

Radiological Work Planning

The inspectors selected the following work activities that had the highest exposure

significance:

ALARA Plan 2013-1-002, Drywell Under-Vessel Activities and Associated Activities

N1R22

ALARA Plan 2013-1-004, Drywell Operations and Local Leak Rate Test Activities

Enclosure

25

ALARA Plan 2013-1-006, Drywell ISI Activities

ALARA Plan 2013-1-007, Recirculation Pump Seals Replacement and Motor PMs

(Numbers 11, 13, and 15)

ALARA Plan 2013-1-010, Drywell Scaffold Activities

ALARA Plan 2013-1-014, Drywell Emergency Relief Valve and Pilot Valve Work

Activities

ALARA Plan 2013-1-024, Main Steam Isolation Valve 01-02 Stem Replacement

Actuator Remove/Replace and Testing

ALARA Plan 2013-1-029, Balance of Plant FAC Activities in RWCU Heat Exchanger

Room and Valve Aisles

ALARA Plan 2013-1-030, Refuel Floor Activities

ALARA Plan 2013-1-031, RWCU Miscellaneous Maintenance, Preventive

Maintenance, Surveillance Testing, Operations N1R22

The inspectors reviewed the ALARA work activity evaluations, exposure estimates, and

exposure reduction requirements. The inspectors determined whether CENG

reasonably grouped the radiological work into work activities based on historical

precedence, industry norms, and/or special circumstances.

The inspectors assessed when CENGs planning identified appropriate dose reduction

techniques, considered alternate dose reduction features, and estimated reasonable

dose goals. The inspectors evaluated whether the ALARA assessment had taken into

account decreased worker efficiency from use of respiratory protective devices and/or

heat stress mitigation equipment. The inspectors determined whether work planning

considered the use of remote technologies as a means to reduce dose and the use of

dose reduction insights from industry operating experience and plant-specific lessons

learned. The inspectors assessed the integration of ALARA requirements into work

procedure and RWP documents.

Verification of Dose Estimates and Exposure Tracking Systems

The inspectors reviewed the assumptions and basis for the current annual collective

dose estimate and outage collective dose estimate for accuracy. The inspectors

reviewed applicable procedures to determine the methodology for estimating exposures

from specific work activities and for department and station collective dose goals.

The inspectors evaluated whether CENG had established measures to track, trend, and

reduce occupational doses for ongoing work activities. The inspectors assessed

whether dose threshold criteria were established to prompt additional reviews and/or

additional ALARA planning and controls.

The inspectors evaluated CENGs method of adjusting exposure estimates or

re-planning work when unexpected changes in scope or emergent work were

encountered. The inspectors assessed whether adjustments to exposure estimates

were based on sound radiation protection and ALARA principles or if they were just

adjusted to account for failures to plan/control the work.

Enclosure

26

Source Term Reduction and Control

The inspectors used station records to determine the historical trends and current status

of plant source term known to contribute to elevated facility collective exposure. The

inspectors assessed whether CENG had made allowances or developed contingency

plans for expected changes in the source term as the result of changes in plant fuel

performance issues or changes in plant primary chemistry.

Radiation Worker Performance

The inspectors observed radiation workers and RPTs performance during refueling

outage activities in radiation areas, airborne radioactivity areas, and high radiation areas.

The inspectors evaluated whether workers demonstrated the ALARA philosophy in

practice and whether there were any procedure or RWP compliance issues.

Problem Identification and Resolution

The inspectors evaluated whether problems associated with ALARA planning and

controls were being identified by CENG at an appropriate threshold and were properly

addressed for resolution in the CENGs CAP.

b. Findings

No findings were identified.

2RS3 In-Plant Airborne Radioactivity Control and Mitigation (71124.03)

a. Inspection Scope

This area was inspected to verify in-plant airborne concentrations were being controlled

consistent with ALARA principles and the use of respiratory protection devices on-site

does not pose an undue risk to the wearer. The inspectors used the requirements in

10 CFR 20, the guidance in RG 8.15, Acceptable Programs for Respiratory Protection,

RG 8.25, Air Sampling in the Workplace, NUREG-0041, Manual of Respiratory

Protection Against Airborne Radioactive Material, TSs, and CENGs procedures

required by TSs as criteria for determining compliance.

Inspection Planning

The inspectors reviewed the UFSAR to identify areas of the plant designed as potential

airborne radiation areas and any associated ventilation systems or airborne monitoring

instrumentation. This review included instruments used to identify changing airborne

radiological conditions such that actions to prevent an overexposure may be taken. The

review included an overview of the respiratory protection program and a description of

the types of devices used. The inspectors reviewed procedures for maintenance,

inspection, and use of respiratory protection equipment as well as procedures for

maintenance and testing of breathing air quality.

Enclosure

27

Engineering Controls

The inspectors reviewed CENGs use of permanent and temporary ventilation to

determine whether CENG uses ventilation systems as part of its engineering controls to

control airborne radioactivity. The inspectors reviewed procedural guidance for use of

installed plant systems to reduce dose and assessed whether the systems are used

during high-risk activities.

The inspectors selected two temporary ventilation system setups on the refuel floor used

to support work in contaminated areas. The inspectors assessed whether the use of

these systems is consistent with procedural guidance and ALARA principles.

The inspectors reviewed airborne monitoring protocols for the drywell and refueling floor

continuous air monitors used to monitor and warn of changing airborne concentrations in

the plant and evaluating whether the alarms and set points are sufficient to prompt

worker action to ensure that doses are maintained within the limits of 10 CFR 20 and the

ALARA concept.

The inspectors assessed whether CENG had established threshold criteria for

evaluating levels of airborne beta-emitting and alpha-emitting radionuclides.

Use of Respiratory Protection Devices

The inspectors selected RWCU repairs and under-vessel control rod drive work activities

where respiratory protection devices were used to limit the intake of radioactive

materials and assessed whether CENG performed an evaluation concluding that further

engineering controls were not practical and that the use of respirators is ALARA. The

inspectors also evaluated whether CENG had established means (such as routine

bioassay) to determine if the level of protection (protection factor) provided by the

respiratory protection devices during use was at least as good as that assumed in work

controls and dose assessment.

Problem Identification and Resolution

The inspectors evaluated whether problems associated with the control and mitigation of

in-plant airborne radioactivity were being identified by CENG at an appropriate threshold

and were properly addressed for resolution in CENGs CAP. The inspectors assessed

whether the corrective actions were appropriate for a selected sample of problems

involving airborne radioactivity and were appropriately documented.

b. Findings

No findings were identified.

2RS4 Occupational Dose Assessment (71124.04)

a. Inspection Scope

From April 22 to 25, 2013, the inspectors reviewed occupational doses to ensure they

were appropriately monitored and assessed. The inspectors used the requirements in

10 CFR 20, RG 8.13, Instruction Concerning Prenatal Radiation Exposure, RG 8.36,

Enclosure

28

Radiation Dose to the Embryo/Fetus, RG 8.40, Methods for Measuring Effective Dose

Equivalent from External Exposure, TSs, and CENGs procedures required by TSs as

criteria for determining compliance.

Inspection Planning

The inspectors reviewed the results of Unit 1 radiation protection program audits related

to internal and external dosimetry. A review was conducted of procedures associated

with dosimetry operations including issuance/use of external dosimetry, assessment of

internal dose, and evaluation of and dose assessment for radiological incidents. The

inspectors evaluated whether CENG had established procedural requirements for

determining when external dosimetry and internal dose assessments are required.

External Dosimetry

The inspectors evaluated whether CENGs dosimetry vendor was accredited with the

National Voluntary Laboratory Accredited Program and if the approved irradiation test

categories for each type of personnel dosimeter used were consistent with the types and

energies of the radiation present and the way the dosimeter is being used.

The inspectors evaluated the onsite storage of dosimeters before issuance, during use,

and before processing and reading. The inspectors also reviewed the guidance

provided to radiation workers with respect to care and storage of dosimeters.

The inspectors assessed the use of electronic personal dosimeters to determine if

CENG uses a correction factor to address the response of the electronic personal

dosimeter as compared to the dosimeter of legal record for situations when the

electronic personal dosimeter is used to assign dose and whether the correction factor is

based on sound technical principles.

The inspectors reviewed two CAP documents for adverse trends related to electronic

personal dosimeters. The inspectors assessed whether CENG had identified any

adverse trends and implemented appropriate corrective actions.

Internal Dosimetry

Routine Bioassay (In Vivo)

The inspectors reviewed procedures used to assess the dose from internally deposited

radionuclides using whole body counting equipment. The inspectors evaluated whether

the procedures addressed methods for differentiating between internal and external

contamination, the release of contaminated individuals, determining the route of intake

and the assignment of dose.

The inspectors reviewed CENGs evaluation for use of its portal radiation monitors as a

passive monitoring system. The inspectors assessed if instrument minimum detectable

activities were adequate to determine the potential for internally deposited radionuclides

sufficient to prompt an investigation.

Enclosure

29

Special Bioassay (In Vitro)

There was no internal dose assessments obtained using whole body count results for

the inspectors to review. There was no internal dose assessments obtained using

urinalysis or fecal sample results for the inspectors to review.

The inspectors reviewed the vendor laboratory quality assurance program and assessed

whether the laboratory participated in an industry-recognized cross check program

including whether out-of-tolerance results were reviewed, evaluated, and resolved

appropriately.

Internal Dose Assessment - Airborne Monitoring

The inspectors reviewed CENGs program for dose assessment based on airborne

monitoring and calculations of derived air concentration calculations. The inspectors

determined whether flow rates and collection times for air sampling equipment were

adequate to allow appropriate lower limits of detection to be obtained. CENG had

performed internal dose assessments using airborne/derived air concentration

monitoring for some work in the cavity during the N1R22.

Internal Dose Assessment - Whole Body Count Analyses

CENG has not documented any internal dose assessments using whole body count

results during the period reviewed.

Special Dosimetry Situations

Declared Pregnant Workers

The inspectors assessed the process used by CENG to inform workers of the risks of

radiation exposure to the embryo/fetus, the regulatory aspects of declaring a pregnancy,

and the specific process to be used for monitoring and controlling exposure to a

declared pregnant worker. CENG has not documented any internal dose assessments

for declared pregnant workers during this inspection period.

Dosimeter Placement and Assessment of Effective Dose Equivalent for External

Exposures

The inspectors reviewed CENGs methodology for monitoring external dose in non-

uniform radiation fields or where large dose gradients exist. The inspectors evaluated

CENGs criteria for determining when alternate monitoring such as use of multi-badging

is to be implemented.

The inspectors reviewed dose assessments performed for workers performing under-

vessel work and RWCU repairs. These workers used multi-badging to evaluate effective

dose equivalent and the dose assessment was performed consistent with CENG

procedures and dosimetry standards.

Enclosure

30

Shallow Dose Equivalent

There were no dose assessments for shallow dose equivalent available for review. The

inspectors evaluated CENGs method for calculating shallow dose equivalent from

distributed skin contamination or discrete radioactive particles.

Assigning Dose of Record

For the special dosimetry situations reviewed in this section, the inspectors assessed

how CENG assigns dose of record for total effective dose equivalent, shallow dose

equivalent, and lens dose equivalent. This included an assessment of external and

internal monitoring results, supplementary information on individual exposures, and

radiation surveys when dose assessment was based on these techniques.

Problem Identification and Resolution

The inspectors assessed whether problems associated with occupational dose

assessment are being identified by CENG at an appropriate threshold and are properly

being addressed for resolution in CENGs CAP. The inspectors assessed the

appropriateness of the corrective actions for a selected sample of problems documented

by CENG involving occupational dose assessment.

b. Findings

No findings were identified.

2RS7 Radiological Environmental Monitoring Program (71124.07)

a. Inspection Scope

From May 6 to 10, 2013, the inspectors verified that the radiological environmental

monitoring program (REMP) quantifies the impact of radioactive effluent released to the

environment and sufficiently validates the integrity of the radioactive gaseous and liquid

effluent release program.

The inspectors used the requirements in 10 CFR 20; 10 CFR 50, Appendix A, Criterion

60, Control of Release of Radioactivity to the Environment; 10 CFR 50, Appendix I,

Numerical Guides for Design Objectives and Limiting Conditions for Operations to Meet

the Criterion As Low As Is Reasonably Achievable for Radioactive Material in Light-

Water-Cooled Nuclear Power Reactor Effluents; 40 CFR 190, Environmental Radiation

Protection Standards for Nuclear Power Operations; 40 CFR 141, Maximum

Contaminant Levels for Radionuclides; RG 1.23, Meteorological Monitoring Programs

for Nuclear Power Plants; RG 4.1, Radiological Environmental Monitoring for Nuclear

Power Plants; RG 4.15, Quality Assurance for Radiological Monitoring Programs;

NUREG-1302, Offsite Dose Calculation Manual Guidance: Standard Radiological

Effluent Controls for Boiling Water Reactors; applicable industry standards; and CENG

procedures as criteria for determining compliance.

Enclosure

31

Inspection Planning

The inspectors reviewed CENGs annual radiological environmental operating reports for

2011 and 2012 and the results of any assessments since the last inspection to verify that

the REMP was implemented and reported in accordance with requirements. This review

included changes to the offsite dose calculation manual (ODCM) in environmental

monitoring, sampling locations, monitoring and measurement frequencies, land-use

census, inter-laboratory comparison program, and analysis of environmental data.

The inspectors reviewed Units 1 and 2 ODCMs to identify locations of environmental

monitoring stations. The inspectors reviewed Units 1 and 2 UFSARs for information

regarding the environmental monitoring program and meteorological monitoring

instrumentation. The inspectors reviewed quality assurance audits and technical

evaluations performed on the vendor analytical laboratory program.

The inspectors reviewed Units 1 and 2 radioactive effluent release reports for 2011 and

2012 and the most recent results from waste stream analysis to determine if CENG was

sampling and analyzing for the predominant radionuclides released in plant effluents.

Site Environmental Inspection

The inspectors walked down five air sampling stations and five environmental thermo

luminescent dosimeter (TLD) monitoring stations to determine whether they were

located as described in the ODCM and to determine the equipment material condition.

For the air samplers and TLD stations selected, the inspectors reviewed the calibration

and maintenance records to verify that they demonstrated adequate operability for these

components. Additionally, the review included the calibration and maintenance records

of four composite water samplers.

The inspectors performed an assessment of any compensatory environmental sampling

upon loss of a required sampling station.

The inspectors observed the collection and preparation of four environmental samples

from surface water and fish to verify that environmental sampling was representative of

the effluent release pathways as specified in the ODCM and that sampling techniques

were in accordance with procedures.

Based on direct observation and review of records, the inspectors assessed whether the

meteorological instruments were operable, calibrated, and maintained in accordance

with procedures. The inspectors assessed whether the meteorological data readout and

recording instruments in the control room and at the meteorological tower were operable

and accurate.

The inspectors evaluated whether missed and/or anomalous environmental samples

were identified and reported in the annual radiological environmental operating reports.

The inspectors selected five events that involved a missed sample or inoperable sampler

to verify that CENG had identified the cause and had implemented corrective actions.

The inspectors reviewed the assessment of any sample results detected above the

lower limits of detection and reviewed CENGs evaluation of associated radioactive

effluent release data that was the potential source of the released material. The 2011

Enclosure

32

radiological environmental operator report noted the detection of Iodine from the

Fukushima Daiichi accident during March and April 2011.

The inspectors selected the following five SSCs that contained licensed material for

which there was a credible mechanism for radioactive material to reach ground water:

Unit 1 drywell, reactor, and turbine building sumps

Unit 2 drywell, reactor, and turbine building sumps

Unit 2 stack condensate transfer line to radwaste

Old radwaste sumps W 11, 12, and 13, and concentrator waste tank cubicle

Waste water treatment facility clarified tanks and sludge pits

The inspectors assessed whether CENG had implemented a sampling, inspection, and

monitoring program to provide early detection of leakage from these SSCs to ground

water.

The inspectors evaluated whether decommissioning records of leaks, spills, and

environmental remediation since the previous inspection were retained in a retrievable

manner in the 10 CFR 50.75(g) decommissioning file. Two records were added to the

decommissioning file in 2012. The first was Unit 1 turbine building roof replacement,

and the second was tritium in-leakage to the Unit 1 screen house.

The inspectors reviewed any significant changes made by CENG to the ODCM as the

result of changes to the land census, long-term meteorological conditions, or

modifications to the sampler stations since the last inspection. The inspectors reviewed

technical justifications for any changed sampling locations to ensure that the changes

did not affect CENGs ability to monitor the impact of plant operations on the

environment.

The inspectors assessed whether the detection sensitivities for environmental samples

were below the lower limits of detection specified in the ODCM. The inspectors

reviewed quality control charts for laboratory radiation measurement instrument and

actions taken for degrading detector performance. The inspectors also reviewed the

results of the vendors quality control program including the inter-laboratory comparison

to assess the adequacy of the vendors program.

The inspectors reviewed the results of Entergy Nuclear Northeast (Entergy) inter-

laboratory and intra-laboratory comparison program to verify the adequacy of

environmental sample analyses performed by James A. Fitzpatrick Nuclear Power Plant

environmental laboratory. The inspectors assessed whether the results included for the

media radionuclide mix was appropriate for the facility.

Identification and Resolution of Problems

The inspectors assessed whether problems associated with the REMP and

meteorological monitoring programs were being identified by CENG at an appropriate

threshold and correction actions were assigned for resolution in CENGs CAP.

Enclosure

33

b. Findings

No findings were identified.

4. OTHER ACTIVITIES

4OA1 Performance Indicator Verification (71151)

RCS Specific Activity and RCS Leak Rate (4 samples)

a. Inspection Scope

The inspectors reviewed CENGs submittal for the RCS specific activity (BI01) and RCS

leak rate (BI02) performance indicators for both Unit 1 and Unit 2 for the period of April

1, 2011, through March 31, 2013. (Note: An additional 12 months of BI02 data was

reviewed due to CENG having updated and revised the BI02 performance indicator data

since the previous inspection.) To determine the accuracy of the performance indicator

reported during those periods, the inspectors used definitions and guidance contained in

Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance

Indicator Guideline, Revision 6. The inspectors also reviewed RCS sample analysis

and control room logs of daily measurements of RCS leakage and compared that

information to the data reported by the performance indicator. Additionally, the

inspectors observed surveillance activities that determined the RCS identified leakage

rate, and chemistry personnel taking and analyzing an RCS sample.

b. Findings

No findings were identified.

4OA2 Problem Identification and Resolution (71152 - 4 samples)

.1 Routine Review of Problem Identification and Resolution Activities

a. Inspection Scope

As required by Inspection Procedure 71152, Problem Identification and Resolution, the

inspectors routinely reviewed issues during baseline inspection activities and plant

status reviews to verify that CENG entered issues into the CAP at an appropriate

threshold, gave adequate attention to timely corrective actions, and identified and

addressed adverse trends. In order to assist with the identification of repetitive

equipment failures and specific human performance issues for follow-up, the inspectors

performed a daily screening of items entered into the CAP.

b. Findings

No findings were identified.

Enclosure

34

.2 Semi-Annual Trend Review

a. Inspection Scope

The inspectors performed a semi-annual review of site issues, as required by Inspection

Procedure 71152 to identify trends that might indicate the existence of more significant

safety issues. In this review, the inspectors included repetitive or closely related issues

that may have been documented by CENG outside of the CAP such as trend reports,

performance indicators, major equipment problem lists, system health reports,

maintenance rule assessments, and maintenance or CAP backlogs. The inspectors also

reviewed CENGs CAP database for the first and second quarters of 2013 to assess

condition reports written in various subject areas (equipment problems, human

performance issues, etc.) as well as individual issues identified during the NRCs daily

condition report review (Section 4OA2.1). The inspectors reviewed CENGs quarterly

trend report for the first quarter of 2013 conducted under CNG-QL-1.01-1008, Periodic

QPA Performance Reporting Process, Revision 00500, to verify that CENG personnel

were appropriately evaluating and trending adverse conditions in accordance with

applicable procedures.

b. Findings and Observations

No findings were identified.

Two trends were identified by the inspectors that had not been identified by CENG.

The inspectors noted a negative trend in the reliability and availability of the emergency

core cooling system (ECCS) keep-fill pumps on Unit 2. The low-pressure core spray

keep-fill pump 2CLS*P2 failed on January 9, 2013, due to motor overload (CR-2013-

000218). On February 28, the HPCS keep-fill pump suddenly failed (CR-2013-001633).

As part of an extent-of-condition review for the low-pressure core spray keep-fill pump

failing, operators identified that Division II RHR system keep-fill pump 2RHS*P2 motor

had an abnormal noise. On April 12, CENG replaced 2RHS*P2 motor. The ECCS

keep-fill pumps are Goulds Pump Model 3196ST with 215T Westinghouse motors rated

for 575 volts. Westinghouse investigations determined that each motor had a turn-to-

turn failure. The failure of the HPCS keep-fill pump resulted in Licensee Event Report

(LER) 2013-002, Failure of High-Pressure Core Spray System Pressure Pump due to a

Motor Winding Failure, in accordance with 10 CFR Part 50.73(a)(2)(v)(D) and 10 CFR

Part 21. All three keep-fill pump motors have been replaced, and CENG has entered

these issues into their CAP as noted by the condition reports above.

The inspectors noted a decrease in the reliability of the Unit 1 RB sumps, and as a

result, an increase in the number of emergency operating procedure entries by control

room operators due to sump failures. The decrease in reliability was noted by three

separate events regarding Unit 1 RB sumps that resulted in emergency operating

procedure entries. These events occurred on January 20, April 12, and April 24, and

were documented in CR-2013-000532, CR-2013-002743 and CR-2013-003371,

respectively. The inspectors review identified that although CENG had properly

assessed sump performance per the NRC maintenance rule 10 CFR 50.65 for the train

level criteria, CENG did not assess sump performance against the system level criteria.

CENG documented this issue in CR-2013-004828 and entered this issue into their CAP.

A subsequent CENG evaluation determined the RB floor and equipment sumps had

exceeded their performance monitoring group functional failure criteria and the systems

Enclosure

35

were placed into (a)(1) status. The inspectors determined that this issue was not more

than minor because the train level criteria were appropriately being monitored and

placing the RB sumps into (a)(1) status for exceeding system level criteria would not

have resulted in additional maintenance-related corrective actions being taken by

CENG.

.3 Annual Sample: Review of Repetitive Valve Packing Leakage Issues

a. Inspection Scope

The inspectors performed an in-depth review of CENGs root cause analysis and

corrective actions associated with CR-2011-007171 and CR-2011-010906 regarding two

forced shutdowns of Unit 2 due to excessive unidentified leak rates in 2011. The

inspectors focused on the implementation of corrective actions and extent-of-condition

and cause reviews as it applied to both units.

The inspectors assessed CENGs problem identification threshold, cause analyses,

extent-of-condition reviews, compensatory actions, and the prioritization and timeliness

of CENGs corrective actions to determine whether CENG was appropriately identifying,

characterizing, and correcting problems associated with this issue and whether the

planned or completed corrective actions were appropriate. The inspectors compared the

actions taken to the requirements of CENGs CAP and 10 CFR 50, Appendix B. In

addition, the inspectors performed field walkdowns and interviewed engineering

personnel to assess the effectiveness of the implemented corrective actions.

b. Findings and Observations

No findings were identified.

On August 6 and December 9, 2011, Unit 2 conducted forced shutdowns due to

excessive unidentified leakage rate. In both cases, the increased unidentified leakage

was determined to be from the failure of the recirculation discharge gate valve,

2RCS*MOV18A. CENG completed separate root cause analysis for both events and

determined the August 6 event was due to a design issue which subjects the packing to

excessive vibrations due to the valve gate being exposed to RCS system flow. The

December 9 event was determined to be the result of a workmanship error following the

August 6 event which resulted in a burr forming on the valve stem and eventually led to

the second packing failure.

The inspectors reviewed the root cause analysis and the ECP associated with the 2001

change in packing design for this valve. The inspectors reviewed photos and drawings

of the valve and interviewed engineering personnel. The inspectors concluded that

CENGs determination of the root cause and major contributing causes were reasonable

and had a sound technical basis. The inspectors also determined that corrective actions

for the August 6 event would not have been expected to preclude the December 9 event.

The inspectors reviewed CENGs extent-of-condition reviews and corrective actions

related to similar valves on both Units 1 and 2. The inspectors concluded that CENG

conducted an appropriate extent-of-condition review and identified other valves which

Enclosure

36

may be susceptible to the same failure mechanism. CENG also developed corrective

actions to enhance their valve packing program and designated an engineer to oversee

this program.

The inspectors conducted an independent review of condition reports from 2000 until the

present looking for excessive leakage issues associated with valve packing. The

inspectors confirmed that a large percentage of issues prior to 2001 and since 2007

have been related to RCS*MOV18A and the underlying design vulnerability. Corrective

actions related to this issue included enhancing torque specification values for the

packing, developing preventive maintenance items to re-torque the packing periodically,

and revising work packages. The inspectors determined these corrective actions were

reasonable and had been implemented appropriately and in a timely manner.

The inspectors also observed that appropriate effectiveness reviews were either

completed or were scheduled to be completed in a timely manner.

.4 Annual Sample: Human Performance Safety Culture Themes

a. Inspection Scope

This inspection focused on CENGs evaluation and resolution of an emerging theme in

the number of human performance cross-cutting issues associated with NRC inspection

findings. Specifically, in the third quarter of 2012, four NRC Green inspection findings

across multiple cornerstones were identified as having common cross-cutting aspects in

the area of Human Performance, Resources, H.2(c), because CENG did not provide

complete, accurate, and up-to-date procedures that were adequate to assure nuclear

safety. On August 9, 2012, CENG initiated CR-2012-007529 and performed an

apparent cause evaluation to assess this trend. The NRC completed Inspection

Procedure 71152 in the form of a problem identification and resolution annual sample to

assess this trend during the fourth quarter of 2012 to provide information to support the

end of cycle assessment. Subsequently, on November 7, CENG initiated CR-2012-

010211, A Cross-Cutting Theme Exists in the Aspect of Human Performance,

Resources, Documentation H.2(c), to further assess and address this adverse trend.

A root cause analysis was completed and corrective actions were recommended for

implementation. The inspectors selected this emerging trend for further review to

develop more recent insights into CENGs progress in addressing the cross-cutting

theme to provide meaningful input to the mid-cycle assessment process. The inspectors

reviewed CENG condition reports, the root cause evaluation, and corrective, preventive,

and compensatory actions associated with the emerging theme. The inspectors also

interviewed plant personnel. The four findings associated with cross-cutting theme

H.2(c) are summarized as follows:

Unit 1 - Inadequate torque applied to SDC isolation valve closure bolts (CR-2012-

001441)

Unit 2 - Loss of SFP cooling due an inadequate procedure (CR-2012-004850)

Unit 2 - Inadequate special operating procedure for loss of SFP cooling (CR-2012-

007811)

Unit 2 - Inadequate evaluation and implementation of design modification to the

turbine gland seal supply system (CR-2012-006615)

Enclosure

37

b. Findings and Observations

No findings were identified.

CENG identified an adverse trend existed in the cross-cutting aspect H.2(c) and

recognized that the theme affected broad areas of performance as assessed in the

fourth quarter of 2012. CENG completed the root cause assessment for the adverse

trend in the H.2(c) cross-cutting aspect in December 2012. The root cause analysis

evaluated the four Green findings and also independently determined the common

causes of these findings.

CENG concluded that the work and administrative control documents and processes

were adequate, but the implementation of these processes was not adequate. Formal

techniques were used to reach this conclusion. The 46 specific causal factors from the

four findings were generalized into 13 general causal areas which were further

condensed (or binned) into five causal themes. The process of generalization of the

causal factors resulted in the majority of causal factors (53 percent) having the theme of

lack of engineering /challenge assumptions /mindset (willingness to accept answer with

no challenge). CENG further concluded a less rigorous standard resulted in products

that were of insufficient quality. The error drivers may be both process and behavior;

however, the results of the common cause analyses did not indicate that process

problems were significant errors.

CENG determined that the root cause of the trend was that site leadership had not

identified marginal performance relative to the technical rigor in the production of work

execution documents and, as such, has not put in place corresponding corrective or

mitigating strategies. A contributing cause was listed that existing administrative

controls governing changes to work orders and reviews of said changes are too lenient

to ensure high quality documents are consistently prepared to support plant operations

and maintenance activities.

The root cause team recommended 22 corrective actions in the report. CENG

management translated these recommendations into 20 unique corrective actions to be

implemented, 18 of which had been completed by the end of the first quarter 2013. The

two remaining corrective actions were to complete quarterly effectiveness reviews and a

final effectiveness review. The assigned corrective action to prevent recurrence

(CAPR159) was formulated to develop and communicate a station policy addressing

work documentation quality.

The corrective actions focused substantially on training plant personnel to properly

implement their procedures and to hold them accountable if they did not follow the

procedures. Three of the recommended corrective actions involved development of or

changes to work procedures. CA #59 was to define the term skill of the craft in a

procedure and was completed on June 12, using guidance obtained from an industry

group; CA #55 was to develop and implement a fleet conduct of engineering

administrative procedure and was closed to CA #244 to reinforce current expectations

for engineering roles and responsibilities; and CA #64 was to develop a process tool to

assist in screening pen and ink changes to procedures. This corrective action was also

changed to revise site procedures to add a requirement to initiate a condition report if a

procedure could not be completed as written. All but one corrective action relied on

knowledge-based corrective actions. The only rule-based corrective action was CA #59.

Enclosure

38

Although the majority of the corrective actions were knowledge-based activities that

relied upon one-time training presentations, only two corrective actions were

implemented to conduct a needs analysis for the specified training. The needs analysis

for CA #58 (improve the use of SDS-006 for bolt-torque requirements) and CA #164

(understanding the work order process) both concluded that no additional or recurring

training were required. The one-time training that had been administered would be

sufficient to correct the adverse trend. As a result, no changes to the initial site training

program will be made and these training topics will not be refreshed periodically during

proficiency training.

The inspectors noted the implemented corrective actions rely almost entirely upon a

series of one-time training activities to result in institutionalized changes to personnel

behavior and organizational culture into the future. Therefore, the effectiveness of the

corrective actions could diminish over time as personnel turnover occurs.

The effectiveness reviews for the corrective actions are scheduled to start in the third

quarter of 2013. There have been no effectiveness reviews completed on the efficacy of

the corrective actions for this cross-cutting aspect theme as of June 2013.

The inspectors could not conclude that CENGs root cause analysis and resultant

corrective actions are correct and effective since they have only recently been fully

implemented. However, the number of findings with a cross-cutting aspect in procedure

adequacy has declined from four to two from the end of cycle to mid cycle NRC reviews.

.5 Annual Sample: Battery Low Specific Gravities

a. Inspection Scope

The inspectors performed an in-depth review of CENGs evaluations and corrective

actions associated with low-specific gravity in the safety-related station batteries.

Specifically, an adverse trend of low-specific gravity readings for cells in all three

safety-related 125 volts direct current (VDC) station batteries at Unit 2 were identified in

CR-2012-001315.

The inspectors assessed CENGs problem identification threshold, extent-of-condition

reviews, compensatory actions, and the prioritization and timeliness of CENGs

corrective actions to determine whether CENG was appropriately identifying,

characterizing, and correcting problems associated with this issue and whether the

planned and completed corrective actions were appropriate. The inspectors compared

the actions taken to the requirements of 10 CFR 50, Appendix B. In addition, the

inspectors performed field walkdowns and interviewed engineering personnel to assess

the effectiveness of the implemented corrective actions.

b. Findings and Observations

CENG determined the most probable cause of the low-specific gravities was that the

battery vendors had removed some electrolyte prior to shipping the battery cells to

NMPNS; and then once at NMPNS, water was added to the cells that diluted the

concentration of sulfuric acid.

Enclosure

39

CENG performed a thorough review of the low-specific gravity issue and obtained

information from the battery vendors to support the probable cause. Corrective actions

included adjusting the method for calculating specific gravity and evaluating adding

electrolyte to restore the specific gravity to the manufacturers recommended level.

CENG verified, based on surveillance testing, that although the specific gravities were

lower than normal, the concentration of sulfuric acid was adequate to obtain sufficient

battery capacity to meet the design basis requirements of the batteries.

The inspectors reviewed condition reports, selected battery test results, and

correspondence from the battery vendors regarding the low-specific gravity issue. The

inspectors determined CENGs overall response to the issue was commensurate with

the safety significance, was timely and included appropriate compensatory actions. The

inspectors determined that the actions taken were reasonable to resolve the low-specific

gravity issue. As part of the review, the inspectors determined that two findings existed

as described below.

b.1 Inadequate Procedural Implementation for Battery Cell Replacement

Introduction. The inspectors identified a Green NCV of 10 CFR 50, Appendix B,

Criterion V, Instructions, Procedures, and Drawings, because CENG did not assure

that the replacement of cells in battery 2C was prescribed and performed by appropriate

procedures which resulted in degraded accuracy of test results and potential degradation

to safety-related battery cells.

Description. The Division III emergency battery bank, battery 2C, at Unit 2 uses jars that

contain three cells each to provide reliable direct current (DC) power for essential DC

loads required during normal and abnormal conditions. CENG determined that two jars

required replacing (a total of six cells). In preparation for this activity, CENG procured

three jars and stored them in the warehouse. The inspectors determined that several

procedural inadequacies existed during storage and subsequent cell replacement.

The cells in the warehouse were not monitored or maintained in accordance with vendor

recommendations. Specifically, the vendor requires that cells stored in spaces that are

not air conditioned should have individual cell voltages checked monthly and charged

when needed to prevent excessive discharge. Although CENG had previously noted

their poor practices with regards to battery storage and has ongoing corrective actions to

provide better storage facilities (as documented in CR-2010-012200), CENG did not take

action to adequately monitor cells in the warehouse. As a result, when the three jars for

battery 2C were obtained from the warehouse, one was found to be visibly sulfated and

had to be discarded, and the other two were found undercharged. Sulfation is an

indication of chronic undercharging and eventually results in permanent loss of capacity.

Although CR-2012-010907 identified the poor condition of the cells, the cell replacement

was continued with potentially degraded cells.

The newly installed cells were not charged prior to or upon installation. This is required

in the vendor manual and the station battery cell replacement procedure, N2-EMP-GEN-

673, 24/48 VDC and 125 VDC Batteries - Cell and Connector Replacement, Revision

00400.

Battery 2C was then subjected to a modified performance test with the newly installed

and uncharged cells. This resulted in over-discharging the new cells. Of the new cells,

Enclosure

40

the two lowest reached 0.903 VDC and 1.167 VDC as opposed to the expected end

voltage of approximately 1.75 VDC. This resulted in a battery capacity of 95 percent. In

comparison a normal battery at the age of battery 2C would have a capacity of

approximately 105 percent. Using uncharged cells artificially lowered the test results

which diminished the ability to use the test results for future trending and could mask

poor performance of the remaining cells.

Finally, after the modified performance test, one of the new cells did not recharge

properly. Specifically the vendor states that an equalization charge should be performed

until the lowest cell is within 0.05 volt of the average of all of the cells. During the

equalization charge for battery 2C after the modified performance test, one of the new

cells did not rise to within 0.05 volt of the average of all of the cells. Although CR-2012-

010901 recognized that the acceptance criteria had not been met, the acceptance

criteria was determined to be unnecessary. CENG did not recognize that the failure to

recharge properly was an indication that the previous procedural inadequacies may have

degraded the cell.

CENG entered these inspector-identified issues into the CAP as CR-2013-005235.

CENG corrective actions included reviewing the previous battery 2C test results and the

work order for the next scheduled modified performance test and verifying battery 2C will

remain operable until the next test scheduled for September 2013. CENG also initiated

CR-2013-005074 to replace the two newly installed jars.

Analysis. The inspectors determined that the failure to assure that the replacement of

cells in battery 2C was prescribed and performed by appropriate procedures was a

performance deficiency that was reasonably within CENGs ability to foresee and correct

and should have been prevented. This finding was more than minor because it was

associated with the equipment performance attribute of the Mitigating Systems

cornerstone and affected the cornerstone objective of ensuring the availability, reliability,

and capability of systems that respond to initiating events to prevent undesirable

consequences.

In accordance with IMC 0609.04, Initial Characterization of Findings, and Exhibit 2 of

IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power,

issued June 19, 2012, the inspectors determined this finding to be of very low safety

significance (Green) because the performance deficiency was not a design or

qualification deficiency, did not involve an actual loss of safety function, did not represent

actual loss of a safety function of a single train for greater than its TS allowed outage

time, and did not screen as potentially risk significant due to a seismic, flooding, or

severe weather-initiating event.

This finding has a cross-cutting aspect in the area of Human Performance, Decision-

Making Component, because CENG did not use conservative assumptions in decision

making. Specifically, CENG did not monitor the cells in storage, question the adequacy

of the discharged cells, charge the cells prior to installation, or fully evaluate the

implications of the test and recharge results H.1(b).

Enforcement. 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and

Drawings, requires, in part, that activities affecting quality shall be prescribed by

documented instructions, procedures, or drawings of a type appropriate to the

circumstances and shall be accomplished in accordance with these instructions,

Enclosure

41

procedures, or drawings. Contrary to the above, CENG did not assure that the

November 2012 replacement of cells in battery 2C was prescribed and performed by

appropriate procedures which resulted in degraded accuracy of test results and potential

degradation to safety-related battery cells. Because this violation was of very low safety

significance (Green) and has been entered into CENGs CAP (CR-2013-005235), this

violation is being treated as an NCV, consistent with Section 2.3.2 of the NRC

Enforcement Policy. (NCV 05000410/2013003-02, Inadequate Procedural

Implementation for Battery Cell Replacement)

b.2 Inadequate Design Control for Battery 2C

Introduction. The inspectors identified a Green NCV of 10 CFR Part 50, Appendix B,

Criterion III, Design Control, because CENG did not verify the adequacy of the design

with respect to battery 2C. Specifically, by failing to size the battery to the most limiting

time period, the sizing calculation significantly overstated the available design margin.

Description. The Division III emergency battery bank, battery 2C, uses jars that contain

three cells each to provide reliable DC power for essential DC loads required during

normal and abnormal conditions at Unit 2. The inspectors reviewed EC-145,

Verification of Adequacy of Division III Battery 2BYS*BAT2C, Revision 2, to determine

if the calculation appropriately verified the adequacy of the size of the installed battery

2C. The inspectors noted that the calculation evaluated the battery based on two time

periods, a 1-minute period and a 119-minute period. In accordance with Institute of

Electrical and Electronics Engineers (IEEE) Standard 485-1997, IEEE Recommended

Practice for Sizing Lead-Acid Batteries for Stationary Applications, and EC-145, the

battery should be sized based upon the most demanding time period. The inspectors

determined that the sizing was incorrect. Specifically, although EC-145 determined that

the first time period (1 minute) was the most demanding, the battery sizing was based

upon the less demanding second time period (119 minutes).

In response to this issue, CENG agreed that the calculation was incorrect, entered this

issue into their CAP (CR-2013-005117), and evaluated the condition for operability.

CENG performed the battery sizing calculation based upon the correct time period and

determined that the battery capacity margin reduced from 26 percent to negative

11 percent (i.e., the battery was undersized by 11 percent). CENG reduced the battery

design and aging margins from the calculation and were able to increase the capacity

margin to positive 10 percent which demonstrated a reasonable expectation of

operability. The significance of reducing the design margin was that the original

calculation would have permitted modifications to the Division III DC system that could

have actually overloaded the battery. The significance of reducing the aging margin is

that the battery would not have been able to perform its design function as the battery

aged.

The inspectors independently performed battery sizing calculations and agreed with

CENGs results.

Analysis. The inspectors determined that the failure to verify the adequacy of the design

with respect to battery 2C was a performance deficiency that was reasonably within

CENGs ability to foresee and correct and should have been prevented. This finding was

more than minor because it was associated with the design control attribute of the

Enclosure

42

Mitigating Systems cornerstone and affected the cornerstone objective of ensuring the

availability, reliability, and capability of systems that respond to initiating events to

prevent undesirable consequences.

In accordance with IMC 0609.04, Initial Characterization of Findings, and Exhibit 2 of

IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power,

issued June 19, 2012, the inspectors determined this finding is of very low safety

significance (Green) because the performance deficiency was not a design or

qualification deficiency, did not involve an actual loss of safety function, did not represent

actual loss of a safety function of a single train for greater than its TS allowed outage

time, and did not screen as potentially risk-significant due to a seismic, flooding, or

severe weather-initiating event.

This finding did not have a cross-cutting aspect because it was not indicative of current

performance. Specifically, EC-145 was last revised in 2008.

Enforcement. 10 CFR 50, Appendix B, Criterion III, Design Control, states, in part, that

design control measures shall provide for verifying or checking the adequacy of design.

Contrary to the above, from July 17, 2008, to June 12, 2013, CENGs design control

measures had not appropriately verified the adequacy of the design regarding battery

2C. Specifically, by failing to size the battery to the most limiting time period, the sizing

calculation significantly overstated the available design margin. Because this violation

was of very low safety significance (Green) and has been entered into CENGs CAP

(CR-2013-005117), this violation is being treated as an NCV, consistent with Section

2.3.2 of the NRC Enforcement Policy. (NCV 05000410/2013003-03, Inadequate

Design Control for Battery Sizing Calculation)

4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153 - 6 samples)

.1 Plant Events

a. Inspection Scope

For the plant events listed below, the inspectors reviewed and/or observed plant

parameters, reviewed personnel performance, and evaluated performance of mitigating

systems. The inspectors communicated the plant events to appropriate regional

personnel, and compared the event details with criteria contained in IMC 0309,

Reactive Inspection Decision Basis for Reactors, for consideration of potential reactive

inspection activities. As applicable, the inspectors verified that CENG made appropriate

emergency classification assessments and properly reported the event in accordance

with 10 CFR Parts 50.72 and 50.73. The inspectors reviewed CENGs follow-up actions

related to the events to assure that CENG implemented appropriate corrective actions

commensurate with their safety significance.

Unit 1 loss of battery board 12 and SDC on April 16, 2013

Loss of all SDC pumps for 17 minutes on April 16, 2013

Enclosure

43

b. Findings

Introduction. The inspectors documented an apparent violation of Unit 1 TS 6.4.1,

Procedures, because CENG failed to properly restore from a loss of a vital DC bus in

accordance with station off-normal procedures resulting in an unplanned loss of all SDC

when time to boil was less than 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />. Specifically, operators failed to recognize a

potential for loss of SDC during battery bus 12 restoration in accordance with N1-SOP-

47A.1, Loss of DC, Revision 00101, and N1-OP-47A, VDC Power System, Revision

02500.

Description. Unit 1 shut down for a refueling outage on April 15, 2013. On April 16,

Unit 1 was in cold shutdown at 118 degrees Fahrenheit with a temperature band of 110

to 120 degrees Fahrenheit. The reactor vessel head was installed, and the head bolts

were in the process of being detensioned in preparation for reactor cavity flood up and

reactor vessel head removal. Primary containment was open for planned maintenance.

Decay heat removal was via the SDC pump 12. SDC pumps 11 and 13 were secured

with their breakers racked out to the test position for planned loss of offsite power/loss of

coolant accident testing (LOOP/LOCA).

During LOOP/LOCA testing, the SDC pumps and ECCS pumps in train associated with

the bus are racked to their test position. Operators are stationed in the field to restore

these pumps to normal so the pumps are still considered to be available. This is

permitted by NMPNS TSs; however, automatic functions of the pumps are not available

(such as auto start on a low-low reactor vessel level signal).

At 2:45 p.m. on April 16, a contractor walking down a tagout associated with an ERV

modification made an error and opened the breaker cabinet door for the vital DC bus 12.

The vital DC bus 12 cabinet door contains a mechanical interlock which opens battery

breaker 12 and the static battery charger DC output breaker, de-energizing the DC

switchgear when the door is open. Upon opening the breaker cabinet door and hearing

the breakers trip, the contractor realized he was in the incorrect cabinet and immediately

contacted the control room and notified them of the event. The vital bus was considered

protective equipment and a sign on the cabinet door cautioned that the door interlock

would trip the breakers in that cabinet. The loss of the vital DC bus 12 resulted in a

partial loss of indication in the main control room, loss of DC control power for the

associated bus, and a high-temperature trip signal for the SDC 12 being generated.

However, since DC power to the trip solenoid was also lost, the SDC pump 12 continued

to run. The ECCS pumps associated with the #12 bus were inoperable due to loss of

control power.

In response to the event, operators entered procedure N1-SOP-47A, Loss of DC,

Revision 00101. The flowchart in SOP-47A.1 directs the operator to transfer selected

loads normally powered from battery bus 12 to their alternate power supplies and then

directs restoration of the bus. However, a decision was made to not take actions

specified in N1-SOP-47A.1 and pursue restoring the vital DC bus 12 using system

operating procedure N1-OP-47A, 125 VDC Power System, Revision 02500. The

inspectors noted that N1-SOP-47A.1 Section 5.1 contains two caution statements stating

that pump trip signals may have been generated while the bus was de-energized and

those signals must be cleared prior to restoration or a pump trip may occur when the bus

is restored and power is supplied to the DC trip coils. However, neither N1-SOP-47A.1

nor N1-OP-47A contained a list of tripping circuits and tripping actions which are

Enclosure

44

associated with the vital DC bus 12. Operators failed to recognize the bus 12

high-temperature trip signal present on the alarm log and the plant process computer

displays prior to attempting to restore bus 12. The presence of the trip signal was also

indicated by a control room annunciator which was locked-in since the loss of battery

bus 12 at 2:45 p.m.

At 3:45 p.m., field operators attempted to close static battery charger 171A DC output

breaker to restore the battery bus from its alternate power supply. Due to the high-

temperature trip signal already being present on the SDC pump 12, when operators

attempted to close the static battery charger 171A output breaker, the DC trip coil

received enough power to energize the relay and trip the SDC pump 12 just before the

static battery charger 171A output breaker tripped due to the mechanical interlock.

Operators did not immediately recognize that they had lost SDC pump 12 via their

indications at the control panel (i.e.; annunciator, pump current, pump flow). Upon

recognizing the loss of SDC at approximately 3:50 p.m., operators entered N1-SOP-6.1

Loss of SFP/RX Cavity Level/Decay Heat Removal, Revision 00501.

At 3:50 p.m., the control room directed the breakers for SDC pumps 11 and 13 to be

racked to their normal positions and that SDC be restored using the 11 and 13 SDC

pumps. The 11 SDC pump breaker was restored at 4:03 pm and SDC flow was restored

at 4:17 pm when the SDC 11 temperature control valve was opened, restoring cooling

flow to the reactor. Reactor vessel temperature rose from 118 to 145 degrees

Fahrenheit as a result of the loss of SDC. At 5:11 p.m., the normal DC power

distribution lineup was restored.

CENG immediately conducted prompt investigations of both the loss of battery bus 12

and loss of SDC events, entered both events into their CAP as CR-2013-002926 and

CR-2013-002916, and conducted a root cause analysis. CENG determined the root

cause for the loss of SDC was inadequate procedural guidance for restoring the DC

power. Contributing causes included operators proceeding in the face of uncertainty,

management oversight of operations, and inadequate use of operational experience

which could have precluded this event. Corrective actions to prevent recurrence

included a review of operations procedures to ensure those procedures contain

adequate levels of detail to safely recover from the event and restore the system to

normal operation.

Analysis. The inspectors determined that CENGs failure to properly restore the battery

bus 12 in accordance with plant procedures was a performance deficiency that was

reasonably within CENGs ability to foresee and correct and should have been

prevented. The performance deficiency was determined to be more than minor because

the inspectors determined it affected the configuration control aspect of the Initiating

Events cornerstone and adversely affected the associated cornerstone objective to limit

the likelihood of events that upset plant stability and challenge critical safety functions

during shutdown as well as power operations. Specifically, operators failed to recognize

a potential for loss of SDC during battery bus 12 restoration in accordance with N1-SOP-

47A.1, Loss of DC, Revision 00101, and N1-OP-47A, VDC Power System, Revision

02500. This performance deficiency initiated a plant transient, loss of shutdown cooling.

The inspectors evaluated the finding using IMC 0609 Attachment 0609.04, Initial

Characterization of Findings, issued June 19, 2012, and IMC 0609 Appendix G,

Shutdown Operations Significance Determination Process, issued February 28, 2005.

Enclosure

45

IMC 0609 Appendix G Table 1, Losses of Control, states a quantitative analysis is

required for:

Loss of Thermal Margin (PWRs and BWRs)

(Inadvertent change in RCS temperature due to loss of RHR)/(change in temperature

that would cause boiling) > 0.2 (temperature margin to boil)

In this case, RCS temperature changed 27 degrees (145 to 118 degrees Fahrenheit)

and the change in temperature to boiling was 94 degrees (212 to 118 degrees

Fahrenheit). Temperature margin to boil was greater than 0.2 (0.2872); thus, a

quantitative analysis was required. The significance of the finding is designated as To

Be Determined (TBD) until a Phase 3 analysis can be completed by Regional and

Headquarters Senior Reactor Analysts.

The inspectors determined this finding had a cross-cutting aspect in the area of Human

Performance, Resources, because CENG did not ensure that personnel, equipment,

procedures, and other resources were available and adequate to assure nuclear safety -

complete, accurate and up-to-date design documentation, procedures, and work

packages, and correct labeling of components. Specifically, CENG procedures

N1-SOP-47A.1 and N1-OP-47A did not contain adequate guidance to ensure recovery

from a loss of a DC bus would not result in an unexpected plant transient H.2(c).

Enforcement. Unit 1 TS 6.4.1, Procedures, requires, in part, that written procedures

and administrative policies shall be established, implemented, and maintained that meet

or exceed the requirements and recommendations of Sections 5.1 and 5.3 of American

National Standards Institute N18.7-1972 Administrative Controls and Quality Assurance

for the Operational Phase of Nuclear Power Plants, and cover the following activities:

the applicable procedures recommended in RG 1.33, Quality Assurance Program

Requirements (Operation), Appendix A, Typical Procedures for Pressurized-Water

Reactors and Boiling-Water Reactors, dated November 3, 1972. RG 1.33, Appendix A,

Section 4, Procedure for Startup, Operation, and Shutdown of Safety-Related BWR

Systems, requires procedures for onsite DC system, and Section 6, Procedures for

Combating Emergencies and Other Significant Events, requires, in part, procedures for

including loss of electrical power (and/or degraded power sources). CENG procedures

N1-OP-47A, 125 VDC Power System, Revision 02500, and N1-SOP-47A.1, Loss of

DC, Revision 00101, implement this requirement. Contrary to the above, on April 16,

2013, operators were unable to properly implement N1-OP-47 and N1-SOP-47A.1

following a loss of the battery bus 12 resulting in a temporary loss of all decay heat

removal. This issue is being characterized as an apparent violation in accordance with

the NRC's Enforcement Policy, and its final significance will be dispositioned in a

separate future correspondence. (Apparent Violation 05000220/2013003-04,

Improper Bus Restoration Results in a Loss of Shutdown Cooling)

.2 (Closed) LER 05000220/2012-006-00: Technical Specification Required Shutdown Due

to Containment Leakage

a. Inspection Scope

On December 13, 2012, Unit 1 commenced a shutdown after observing nitrogen leakage

from primary containment over a period of 10 days. NRC Inspection Report

Enclosure

46

05000220/2012005 documented CENGs immediate response and the NRCs initial

review of the event. As of the end of the inspection documented in that report, CENGs

evaluation of the causes for the leakage was still ongoing. The inspectors had identified

an issue of concern regarding the total amount of leakage from primary containment

vent and purge valves and its relation to exceeding the required value in TS 3.3.3. The

NRC opened URI 05000220/2012005-03 to track CENGs completion of the root cause

evaluation, the quantification of the amount of leakage from primary containment for the

event, and the NRCs subsequent review of CENGs completed evaluation.

To close URI 05000220/2012005-03 the inspectors reviewed and independently verified

CENGs calculation regarding the quantity of leakage from primary containment from

December 3 - December 13. The inspectors also reviewed Appendix J Type B and C

testing of the primary containment vent and purge valves to determine leakage

quantities and how they impacted overall primary containment leakage. The inspectors

also reviewed the cause of the leakage and CENGs actions to address the cause which

was included in CR-2012-011157. URI 05000220/2012005-03 is closed to the violation

discussed below. The enforcement actions associated with this LER are discussed

below. This LER is closed.

b. Findings

Introduction. A self-revealing Green NCV of TS 3.3.3, Leakage Rate, was identified for

CENGs failure from December 3 to December 13, 2012, to maintain containment

leakage less than 1.5 percent by weight of the containment air per day and less than 0.6

percent by weight of the containment air per day for all penetrations and all primary

containment isolation valves subject to 10 CFR Part 50, Appendix J, Types B and C

tests, when pressurized to 35 pounds per square inch gauge (psig) when RCS

temperature is above 215 degrees Fahrenheit and primary containment integrity is

required.

Description. On December 3, 2012, at 11:31 a.m., Unit 1 established primary

containment integrity and commenced a reactor startup from an unplanned outage. The

following day at 2:40 a.m., CENG operators commenced adding nitrogen gas into the

primary containment as part of a planned activity to reduce primary containment oxygen

concentration to less than 4 percent as required by TS 3.3.1, Oxygen Concentration.

This activity was completed at 10:55 a.m. on December 4. Once an appropriate nitrogen

concentration has been achieved in the containment, additional makeup is generally not

required. However, from December 6 through December 8, on three occasions,

operators added additional nitrogen to the containment to maintain pressure within

procedural limits. This issue was documented in CR-2012-011157, Adverse Trend in

Unit 1 Nitrogen Usage. CENG commenced initial troubleshooting activities which

included examining systems and components that were possible sources of nitrogen

leakage; however, a definitive source for the leakage was not identified. On

December 12, following a fourth addition of nitrogen, CENG increased the importance of

the issue, formed an issue response team, and staffed the outage control center. As

part of the investigation process, operators cycled several containment isolation valves

in the nitrogen purge and vent system and attempted to quantify the amount of seat

leakage through the valves by opening test fittings located between isolation valves. In

parallel with the troubleshooting efforts, CENG and vendor personnel began to develop

analytical tools that could be used to quantify the amount of containment leakage.

Enclosure

47

On December 13, at 6:47 p.m., after observing a decrease in containment pressure

following a fifth nitrogen addition and receiving preliminary data that a containment

isolation valve local leak-rate test between reactor containment inert gas purge and fill

drywell cooling system isolation valves IV-201-31 and IV-201-32 may fail, CENG

commenced a plant shutdown because primary containment integrity as required in TS 3.3.3 could not be assured. On December 13, at 11:33 p.m., the plant reached cold

shutdown and exited plant TS 3.3.3.

Subsequent testing of containment isolation valves revealed that three valves in the

reactor containment inert gas purge and fill drywell cooling system, valves IV-201-10,

IV-201-31, and IV-201-32 had unacceptable seat leak rates. These conditions were

documented in condition reports 2012-011210 and 2012-011288. When the valves were

disassembled and examined, CENG identified that iron oxide (i.e., rust) buildup on the

valve resilient seats had prevented the valves from closing tightly and adversely

impacted seat leakage performance. The reactor containment inert gas purge and fill

drywell cooling system is a carbon steel system and the internal piping surface adjacent

to the valves had visible signs of iron oxide degradation. CENG corrective actions

included removing the loose surface rust, installing new resilient seats on the valves,

and successfully performing as-left local leak-rate tests on the subject valves. Additional

corrective actions were outlined in CR-2012-011247.

CENG analysis determined that based upon the nitrogen supplied to the drywell,

containment leakage from December 3 through December 13, 2012, exceeded the limits

in TS 3.3.3 which requires containment leakage to be less than 1.5 percent by weight of

the containment air per day and less than 0.6 percent by weight of containment air per

day for all penetrations and all primary containment isolation valves subject to 10 CFR Part 50, Appendix J, Types B and C tests, when pressurized to 35 psig when RCS

temperature is above 215°F and primary containment integrity is required. Specifically,

leakage was calculated to be between 1,421 and 2,023 standard cubic feet per hour

verses a calculated limit of 647 standard cubic feet per hour.

Analysis. The inspectors determined that CENGs failure to maintain containment

leakage from December 3 through December 13, 2012, within the limits required by TS 3.3.3 was a performance deficiency that was within CENGs ability to foresee and

correct and should have been prevented. This finding is more than minor because it is

associated with the SSC and barrier performance attribute of the Barrier Integrity

cornerstone and affected the cornerstone objective to provide reasonable assurance that

physical design barriers (fuel cladding, RCS, and containment) to protect the public from

radionuclide releases caused by accidents or events. Specifically, containment leakage

from December 3 through December 13 exceeded the leakage limits outlined in Unit 1

TS 3.3.3.

In accordance with IMC 0609.04, Initial Characterization of Findings, and Table 6.2,

Phase 2 Risk Significance-Type B Findings at Full Power, of IMC 0609, Appendix H,

Containment Integrity Significance Determination Process, issued May 6, 2004, the

inspectors determined this finding was of very low safety significance (Green) because

the leakage was less than 100 percent of containment volume per day for the duration of

the leak.

This finding has a cross-cutting aspect in the area of Problem Identification and

Resolution, CAP, because CENG failed to take appropriate corrective action to address

Enclosure

48

safety issues and adverse trends in a timely manner commensurate with their safety

significance. Specifically, following identification of the adverse trend regarding the

frequency of nitrogen addition to the drywell, CENG did not assess in a timely manner

the significance of the leakage and the impact on primary plant containment. As a

result, plant operation continued for several days with drywell leakage that exceeded the

limits outlined in TS 3.3.3 P.1(d).

Enforcement. TS 3.3.3, Leakage Rate, requires containment leakage to be less than

1.5 percent by weight of the containment air per day and less than 0.6 percent by weight

of the containment air per day for all penetrations and all primary containment isolation

valves subject to 10 CFR Part 50, Appendix J, Types B and C tests, when pressurized

to 35 psig when RCS temperature is above 215 degrees Fahrenheit and primary

containment integrity is required. Contrary to the above, from December 3 through 13,

2012, containment leakage exceeded 1.5 percent by weight. Specifically, following a

December 13 plant shutdown, CENG determined containment leakage during this period

to have been between 1,421 and 2,023 standard cubic feet per hour verses a calculated

limit of 647. Because this violation is of very low safety significance (Green) and CENG

entered this issue into their CAP as CR-2013-011247, this finding is being treated as an

NCV consistent with consistent with Section 2.3.2 of the NRC Enforcement Policy.

(NCV 05000220/2013003-05, Containment Leakage Exceeds Technical

Specification 3.3.3 Limits)

.3 (Closed) LER 05000220/2012-006-01: Technical Specification Required Shutdown Due

to Containment Leakage

This LER was revised on June 14, 2013, to reflect changes in corrective actions that

were outlined in the original LER submittal. In the original LER, CENG indicated that

during the spring 2013 refueling outage, the internal surfaces of the horizontal drywell

vent and purge piping that contained valves IV-201-09, IV-201-10, IV-201-31, and

IV-201-32 would be coated with a material that would minimize the recurrence of rust

buildup on the piping. Further, during the outage, the vertical piping that contained

valves IV-201-07, IV-201-08, IV-201-16, and IV-201-17 would be inspected; and based

on the inspection findings, a coating strategy (if required) would be developed for that

piping. Subsequent to submittal of the original LER, CENG determined that based upon

the difficultly associated with application of a suitable coating to the pipes and the

potential of subsequent coating failure, a protective coating would not be installed.

In lieu of the original corrective actions, CENG indicated that the horizontal section of

pipe would be inspected each refueling outage. The vertical piping would not be

inspected. These corrective actions were based, in part, on results from inspections

conducted during the 2013 N1R22 that identified rust accumulation only on the

horizontal sections of pipe. The enforcement aspects of this issue are discussed in

section 4OA3.2 of this report. The inspectors did not identify any new issues during the

review of this revised LER. This LER is closed.

.4 (Closed) LER 05000220/2012-007-00: High-Pressure Coolant Injection System Logic

Actuation Following an Automatic Turbine Trip Signal due to High Reactor Water Level

On November 6, 2012, while Unit 1 was in cold shutdown, an unexpected rise in reactor

water level occurred causing an automatic turbine trip signal and actuation of the

high-pressure coolant injection initiation logic. Operators immediately closed the 12

Enclosure

49

feedwater pump discharge blocking valve and stabilized reactor water level, stopping the

transient. At Unit 1, high-pressure coolant injection is a mode of operation of the

condensate and feedwater system that utilizes the condensate storage tanks, main

condenser hotwell, two condensate pumps, two feedwater booster pumps, and two

motor-driven feedwater pumps. The rise in reactor water level resulted from the 12

feedwater flow control valve (FCV) FCV-29-137 unexpectedly failing partially open when

instrument air was removed from the valve during a tagout in preparation for

maintenance on the valve. FCV-29-137 has a series of lockup valves that are designed

to hold the FCV stem in position in the event instrument air is lost. CENG determined

FCV-29-137 partially opened due to a degraded top cylinder lockup valve O-ring. The

enforcement aspects of this issue are discussed in NRC Integrated Inspection Report 05000220/2013002, Section 1R22. The inspectors did not identify any new issues

during the review of the LER. This LER is closed.

.5 (Closed) LER 05000410/2013-001-00: Reactor Core Isolation Cooling System Isolation

Due to a Temperature Switch Unit Failure

On January 23, 2013, at 3:16 p.m., Unit 2 was operating at 100 percent power when an

unexpected isolation signal for containment isolation valves in the RCIC and RHR

system occurred due to a failure of a RB general area temperature switch

(2RHS*TS85A). The isolation resulted in the RCIC system being unavailable for

injection into the reactor vessel if called upon during an event. The affected RHR

isolation valves were already in the closed position which is their normal position during

power operation. The failure also occurred concurrently with the HPCS system being

inoperable for planned surveillance testing. With both RCIC and HPCS inoperable,

high-pressure coolant makeup capability was lost. At 3:50 p.m., HPCS was restored

and declared operable. Temperature switch 2RHS*TS85A was replaced at 11:04 p.m.,

and on January 24, at 1:17 a.m., RCIC was declared operable. The cause of the

temperature switch failure was determined to be age-related capacitor degradation. The

enforcement aspects of this issue are discussed in NRC Integrated Inspection Report 05000410/2013002, Section 1R12. The inspectors did not identify any new issues

during the review of the LER. This LER is closed.

.6 (Closed) LER 05000410/2013-002-00: Failure of High-Pressure Core Spray System

Pressure Pump Due to Motor Winding Failure

On February 28, 2013, Unit 2 was operating at 100 percent power when the HPCS

system pressure pump failed. At the time of the failure, the HPCS system was

inoperable for planned maintenance. The pump failure was due to turn-to-turn short in

the motor winding. The HPCS system pressure pump is designed to maintain a positive

pressure on the HPCS discharge header to prevent voids from forming. CENG replaced

the HPCS pressure pump motor and returned the HPCS system to an operable status

on March 6. The HPCS system discharge piping remained full during the period when

the pressure pump was OOS. The inspectors reviewed the maintenance history of the

HPCS pressure pump motor and determined that when the motor bearings were

replaced in January 2011, the work order documented a satisfactory visual inspection

and meggar testing of the motor windings. The inspectors reviewed the LER and

determined that no findings or violations of NRC requirements were identified. This LER

is closed.

Enclosure

50

4OA6 Meetings, Including Exit

Exit Meeting

On July 25, 2013, the inspectors presented the inspection results to Mr. Christopher

Costanzo, Site Vice President, and other members of the NMPNS staff. The inspectors

verified that no propriety information was retained by the inspectors or documented in

this report.

ATTACHMENT: SUPPLEMENTARY INFORMATION

Enclosure

A-1

SUPPLEMENTARY INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

C. Costanzo, Vice President

J. Stanley, Plant General Manager

P. Bartolini, Supervisor, Design Engineering

K. Clark, Director, Security

S. Dack, Seasonal Readiness Coordinator / Cycle Manager

J. Dean, Supervisor, Quality Assurance

S. Dhar, Design Engineering

J. Dosa, Director, Licensing

J. Gillard, Emergency Preparedness Analyst

J. Holton, Supervisor, Systems Engineering

G. Inch, Principle Engineer,

M. Kunzwiler, Security Supervisor

J. Leonard, Supervisor Design Engineering

C. McClay, Senior Engineer

F. Payne, Manager, Operations

P. Politzi, Work Week Manager

J. Reid, Design Engineer

B. Scaglione, System Engineer

J. Schulz, System Engineer

M. Shanbhag, Licensing Engineer

R. Staley, System Engineer

T. Syrell, Manager, Nuclear Safety and Security

J. Thompson, General Supervisor, Mechanical Maintenance

A. Verno, Director, Emergency Preparedness

Attachment

A-2

LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED

Opened

05000220/2013003-04 AV Improper Bus Restoration Results in a Loss of

Shutdown Cooling (Section 4OA3)

Opened/Closed

05000410/2013003-01 NCV Failure to Follow Containment Isolation System

Surveillance Procedure Resulting in Isolation of the

Reactor Coolant Isolation Cooling System

(Section 1R22)05000410/2013003-02 NCV Inadequate Procedural Implementation for Battery

Cell Replacement (Section 4OA2)05000410/2013003-03 NCV Inadequate Design Control for Battery Sizing

Calculation (Section 4OA2)05000220/2013003-05 NCV Containment Leakage Exceeds Technical

Specification 3.3.3 Limits (Section 4OA3)

Closed

05000220/2012005-03 URI Assessment of Containment Leakage Due to

Containment Isolation Valve Failure (4OA3)

05000220/2012-006-00 and LER Technical Specification Required Shutdown Due

05000220/2012-006-01 to Containment Leakage (Section 4OA3)

05000220/2012-007-00 LER High-Pressure Coolant Injection System Logic

Actuation Following an Automatic Turbine Trip

Signal Due to High Reactor Water Level

(Section 4OA3)

05000410/2013-001-00 LER Reactor Core Isolation Cooling System Isolation

Due to a Temperature Switch Unit Failure

(Section 4OA3)

05000410/2013-002-00 LER Failure of High-Pressure Core Spray System

Pressure Pump Due to Motor Winding Failure

(Section 4OA3)

Attachment

A-3

LIST OF DOCUMENTS REVIEWED

Section 1R01: Adverse Weather Protection

Procedures

N1-OP-64, Meteorological Monitoring, Revision 00603

N2-OP-102, Meteorological Monitoring, Revision 01103

N2-OP-102, Attachment 3, Hot Weather Preparation Checklist, Revision 01102

NAI-PSH-11, Seasonal Readiness Program, Revision 00700

Condition Reports

CR-2010-008430 CR-2011-010519 CR-2012-004448

CR-2011-008564 CR-2012-001034 CR-2012-007341

CR-2011-009058 CR-2012-002008 CR-2013-000154

CR-2011-009946 CR-2012-004258

Work Orders

WO C90679919 WO C91901545 WO C92110489

WO C91178423 WO C91919260 WO C92116209

WO C91425002 WO C91920244 WO C92133487

WO C91570604 WO C91966877 WO C92135500

WO C91570606 WO C92033133 WO C92139868

WO C91711577 WO C92008152 WO C92154168

WO C91847825 WO C92008169 WO C92156668

WO C91860534 WO C92015166 WO C92156894

WO C91862547 WO C92044771 WO C92161257

WO C91862559 WO C92067054 WO C92221738

WO C91883258 WO C92073630 WO C92226912

WO C91883511 WO C92073671 WO C92285675

WO C91883613 WO C92073704 WO C92292596

WO C91897710 WO C92107827

Miscellaneous

Diesel Trend Analysis

Summer Readiness Status, Attachment 1

System Seasonal Readiness Evaluations, Attachment 2

Unit 1 Scheduler Evaluation for Summer Readiness from June 15 to September 15

Unit 2 Scheduler Evaluation for Summer Readiness from June 15 to September 15

Section 1R04: Equipment Alignment

Procedures

N1-OP-13, Emergency Cooling System, Revision 03700

N1-OP-48, Control Room Ventilation System, Revision 02400

NIP-OUT-01, Shutdown Safety, Revision 03700

Attachment

A-4

Condition Reports

CR-2013-004333

CR-2013-004347

Drawings

B-69017-C, Emergency Condenser Number 11 Steam Flow, Revision 1

C-180007-C, Reactor Core Spray Piping and Instrumentation Drawing (P&ID), Revision 58

C-18008-C, Spent Fuel Storage Pool Filtering and Cooling System, Revision 38

C-18030-C, Fire Protection Water System, Revision 38

C-18047-C, Control Room Heating Ventilation and Air Conditioning System, Revision 48

C-181017-C, Emergency Cooling System, Revision, Revision 55

Miscellaneous

Plant Configuration Change 1M00888

Section 1R05: Fire Protection

Procedure

N1-PFP-0101, Unit 1 Pre-Fire Plans, Revision 00200

Condition Report

CR-2013-002902

Miscellaneous

USAR Section 10, Revision 16

Section 1R07: Heat Sink Performance

Procedure

N1-ST-Q25, Emergency Diesel Generator Cooling Water Quarterly Test, Revision 02201

Work Order

WO C91454468

Section 1R08: In-Service Inspection

Procedures

NDEP-PT-3.00, Liquid Penetrant Examination, Revision 01900

NDEP-UT-6.23, UT Examination of Ferritic Piping Welds, Revision 01100

NDEP-UT-6.24, UT Examination of Austenitic Piping Welds, Revision 01101

NDEP-VT-2.01, ASME Section XI Visual Examination, Revision 19

NDEP-VT-2.07, In-Vessel Visual Examination, Revision 1300

NIP-IIT-02, ASME Section XI Repair and Replacement Program, Revision 00701

SI-UT-130, Phased Array Ultrasonic Examination of Dissimilar Metal Welds, Revision 0

Condition Reports

CR-2012-000816

Attachment

A-5

CR-2012-003805

CR-2012-010291

CR-2013-000506

CR-2013-001573

CR-2013-002975

CR-2013-002977

CR-2013-002978

CR-2013-003442

Drawing

C-18009, Reactor Water Cleanup P&ID, Revision 60, Sheet 1

Work Order

WO C92260831

NDE Records

BOP-UT-13-014, UT Calibration/Thickness Examination Records of RBCLC System Piping to

Recirculation Pump 11 Motor MOT-32-187, dated April 21, 2013

BOP-UT-13-015, UT Calibration/Thickness Examination Records of RBCLC System Piping to

Recirculation Pump 12 Motor MOT-32-188, dated April 21, 2013

BOP-UT-13-016, UT Calibration/Thickness Examination Records of RBCLC System Piping to

Recirculation Pump 13 Motor MOT-32-189, dated April 21, 2013

BOP-UT-13-017, UT Calibration/Thickness Examination Records of RBCLC System Piping to

Recirculation Pump 14 Motor MOT-32-190, dated April 21, 2013

BOP-UT-13-018, UT Calibration/Thickness Examination Records of RBCLC System Piping to

Recirculation Pump 15 Motor MOT-32-191, dated April 21, 2013

BOP-UT-13-021, UT Calibration/Thickness Examination Records of General Corrosion of

RBCLC System Piping Inside U1 Drywell 225 Feet Elevation, dated April 24, 2013

ISI-PT-13-003, Liquid Penetrant Examination Record of Branch Connection - Decontamination

Port Weld 32-WD-011 on Recirculation System Suction Piping, dated April 24, 2013

ISI-PT-13-004, Liquid Penetrant Examination Record of Branch Connection - Decontamination

Port Weld 32-WD-091 on Recirculation System Suction Piping, dated April 24, 2013

ISI-UT-13-032, UT Calibration/Examination Records of Branch Connection - Decontamination

Port Weld 32-WD-051 on Recirculation System Suction Piping, dated April 22, 2013

ISI-UT-13-033, UT Calibration/Examination Records of 12-Inch Diameter Emergency Condenser

Supply Piping, Pipe-to-Pipe Weld 39-WD-108, dated April 24, 2013

ISI-UT-13-034, UT Calibration/Examination Records of 12-Inch Diameter Emergency Condenser

Supply Piping, Pipe-to-Tee Weld 39-WD-109, dated April 24, 2013

ISI-UT-13-035, UT Calibration/Examination records of 12-Inch Diameter Emergency Condenser

Supply Piping, Tee-to-Pipe Weld 39-WD-110, dated April 24, 2013

ISI-UT-13-036, UT Calibration/Examination Records of 12-Inch Diameter Emergency Condenser

Supply Piping, Pipe-to-Elbow Weld 39-WD-112, dated April 20, 2013

NMP U1 33-WD-046, Phased Array UT Calibration/Examination Records of 6-Inch Diameter

RBCLC Pipe-to-Pipe DM Weld, dated April 29, 2013

UT Calibration/Examination Records of Unit 1 32-WD-042, N2A Safe End-Nozzle DM Weld,

Phased Array Ultrasonic Examination Record, dated April 30, 2013

UT Calibration/Examination Records of Unit 1 32-WD-042, N2A Safe End-to-Nozzle DM Weld

on Recirc Discharge, Phased Array Ultrasonic Examination Record, dated April 30, 2013

UT Calibration/Examination Records of Unit 1 32-WD-082, N2B Safe End-to-Nozzle DM Weld

on Recirc Discharge, Phased Array Ultrasonic Examination Record, dated April 30, 2013

Attachment

A-6

UT Calibration/Examination Records of Uni5 1 32-WD-122, N2C Safe End-to-Nozzle DM Weld

on Recirc Discharge, Phased Array Ultrasonic Examination Record, dated April 30, 2013

UT Calibration/Examination Records of Unit 1 32-WD-164, N2D Safe End-to-Nozzle DM Weld

on Recirc Discharge, Phased Array Ultrasonic Examination Record, dated April 30, 2013

UT Calibration/Examination Records of Unit 1 32-WD-208, N2E Safe End-to-Nozzle DM Weld

on Recirc Discharge, Phased Array Ultrasonic Examination Record, dated April 30, 2013

Miscellaneous

Audit Report SPC-12-01-N, Special Processes, Testing, & Inspection, dated November 28, 2012

ASME, 2004 Edition

Section 1R11: Licensed Operator Requalification Program and Licensed Operator

Performance

Procedure

CNG-OP-1.01-1000, Conduct of Operations, Revision 00900

Condition Reports

CR-2013-002697

CR-2013-002698

CR-2013-002647

CR-2013-002652

Section 1R12: Maintenance Effectiveness

Procedures

CNG-AM-1.01-1023, Maintenance Rule Program, Revision 00201

N2-OP-33, High Pressure Core Spray System, Revision 01201

N2-OSP-CSH-Q@002, HPCS Pump and Valve Operability and System Integrity Test,

Revision 00500

Condition Reports

CR-2011-006564 CR-2012-002176 CR-2012-009400

CR-2011-006930 CR-2012-002198 CR-2012-009982

CR-2011-007084 CR-2012-002249 CR-2012-010499

CR-2011-007313 CR-2012-002711 CR-2013-000159

CR-2011-007654 CR-2012-005017 CR-2013-000563

CR-2011-007830 CR-2012-005119 CR-2013-001491

CR-2011-009790 CR-2012-005999 CR-2013-001633

CR-2011-010817 CR-2012-006141 CR-2013-002768

CR-2012-000359 CR-2012-007193 CR-2013-002945

CR-2012-001459 CR-2012-008548 CR-2013-002969

CR-2012-001614 CR-2012-008816

Miscellaneous

ACE for CR-2011-006930

Attachment

A-7

ACE for CR-2012-002176

Eval-NMP-PRM-03046, (a)(1) Evaluation for 1-PRM-F01

Unit 1 Containment Spray System Health Report, 1st Quarter 2013

Unit 1 Neutron Monitoring System Health Report, 1st Quarter 2013

Unit 1 Service Water System Health Report, 1st Quarter 2013

Unit 2 High-Pressure Core Spray System Health Report, 1st Quarter 2013

Section 1R13: Maintenance Risk Assessments and Emergent Work Control

Procedures

CNG-MN-4.01-1004, On-Line T-Week Process, Revision 00302

N2-ISP-LDS-Q010, Reactor Building General Area Temperature Instrument Channel Functional

Test, Revision 00102

N2-OP-71D, Uninterruptible Power Supplies, Revision 00800

N2-SOP-29.1, Reactor Recirculation Pump Seal Failure, Revision 00101

N2-SOP-97, Reactor Protection Systems Failures, Revision 00401

NIP-OUT-01, Shutdown Safety, Revision 03700

S-ODP-OPS-0122, Posting and Control of Protected Equipment during Online and Outage

Operations, Revision 00500

Condition Reports

CR-2013-002461

CR-2013-002916

CR-2013-002926

CR-2013-002958

CR-2013-002998

CR-2013-005021

CR-2013-005077

Work Orders

WO C90962110

WO C91488068

WO C90648733

Miscellaneous

Control Room Operator Logs for Tuesday April 16, 2013

NIP-OUT-01, Shutdown Safety, Revision 03700, Attachment 1, Shutdown Safety Contingency

Plan (or Equivalent), Contingency Plan No. N1R22-003

NIP-OUT-01, Shutdown Safety, Revision 03700, Attachment 1, Shutdown Safety Contingency

Plan (or Equivalent), Contingency Plan No. N1R22-004

NIP-OUT-01, Shutdown Safety, Revision 03700, Attachment 1, Shutdown Safety Contingency

Plan (or Equivalent), Contingency Plan No. N1R22-005

Outage Control Center Logs for Tuesday April 16, 2013

Work Control Center Turnover Sheet for April 16, 2013, Days to Night.

Section 1R15: Operability Determinations and Functionality Assessments

Procedures

CNG-OP-1.01-1002, Conduct of Operability Determinations/Functionality Assessments,

Attachment

A-8

Revision 00200

N1-IPM-092-100, SRM Detector Drive Maintenance and Limit Switch Calibration, Revision 00700

N1-OP-18, Service Water System, Revision 02902

N1-OP-38A, Source Range Monitor, Revision 02000

N1-ST-C5, Secondary Containment and Reactor Building Emergency Ventilation System

Operability Testing, Revision 01600

N1-ST-C6, Source Range Monitor Operability Test, Revision 01100

Condition Reports

CR-2013-002637 CR-2013-003186 CR-2013-003698

CR-2013-002945 CR-2013-003445 CR-2013-004481

CR-2013-002969 CR-2013-003504 CR-2013-005079

CR-2013-002978 CR-2013-003520 CR-2013-004807

CR-2013-003107 CR-2013-003548

CR- 2013-003116 CR-2013-003567

CR-2013-003124 CR-2013-003589

Drawing

RX-147741, 10HN-18 Refinery Pump Elevation, Revision 0

Documents

UFSAR Section VI-2.0, Secondary Containment, Revision 15

UFSAR Section VII-3.0, Emergency Ventilation System, Revision 18

UFSAR Section VII-B, Containment Spray System, Revision 18

UFSAR Section XVI-2.0, Containment Spray System, Revision 20

Section 1R18: Plant Modifications

Procedure

N2-EPM-GEN-V786, MOD Actuator and Damper PM, Revision 00700

Condition Reports

CR-2013-002334

CR-2013-002303

Drawing

ECN Number ECP-12-000616-CN-004 LR18047C

Work Order

WO C919733104

Miscellaneous

ECP 12-000616, Installation of Bubble Tight Damper (BV-210-36)

ECP 13-000167, Installation of Replacement Pump for Unit 1 Service Water Radiation Monitor

ECP 13-000347, Temporary Change to Plug Hand Wheel Connection for 2HVP*AOD5A

Section 1R19: Post-Maintenance Testing

Attachment

A-9

Procedures

CNG-MN-4.01-1008, Pre-/Post-Maintenance Testing, Revision 00100

N1-FST-FPP-C005, Ventilation/Smoke Purge System, Revision 00400

S-EPM-GEN-063, MOV Diagnostic Testing, Revision 00700

Condition Reports

CR-2013-003051

CR-2013-003251

CR-2013-004003

CR-2013-004052

CR-2013-004177

CR-2013-004212

CR-2013-004253

Drawings

C-19410-C, Elementary Wiring Diagram 4.16 kV Emergency Power Boards and Diesel

Generators (102 and 103 Power Circuits), Revision 28, Sheet 1,

C-22277-C, 4160 Volt Power Board 102 Connection Diagram Unit 2-1, Diesel Generator 102,

Revision 09, Sheet 1

C-19437-C, Elementary Wiring Diagram 600V, Power Board 161B Control Circuits, Revision 25,

Sheet 2

C-19437-C, Elementary Wiring Diagram 600V, Power Board 161B Control Circuits, Revision 25,

Sheet 6

C-19017-C, Emergency Cooling System P&I Diagram, Revision 55, Sheet 1

Work Orders

WO C91473955

WO C91474635

WO C91973104

WO C92264883

WO C92279163

WO C92279776

Miscellaneous

ECP-13-000420-015-9, Removal and Replacement of Existing Cable 102-33 from EDG102 to

Power Board 102, Revision 0000

ECP-12-000575, Standard Spec for Electrical Installation Activities at NMP1, Revision 21.00

N21036, Limitorque Type SMB and SB Instruction and Maintenance Manual, NMPCNO:

N2L20000VALVOP004

SPEC NMP1-325M,Section II, Penetration Seals, Revision 1

Section 1R20: Refueling and Other Outage Activities

Procedures

CNG-OP-3.01-1000, Reactivity Management, Revision 00800

Attachment

A-10

N1-FHP-27C, Core Shuffle, Revision 00603

N1-FHP-25, General Description of Fuel Moves, Revision 02301

N1-OP-43C, Plant Shutdown, Revision 01200

N1-RESP-9, SRM Operability for Core Alterations, Revision 00001

N1-ST-V3, Rod Worth Minimizer Operability Test APRM/IRM Overlap Verification, Revision

01300

Condition Report

CR-2013-002793

Tagout

TO-30-0224

Miscellaneous

RFO22 Fuel Movement Instructions

Section 1R22: Surveillance Testing

Procedures

N1-ISP-LRT-TYC, Type C Containment Isolation Valve Local Leak Rate Test, Revision 00900

N1-ST-C5, Secondary Containment and Reactor Building Emergency Ventilation System

Operability Test, Revision 01600

N1-ST-Q15, Condensate Transfer System Operability Test, Revision 00703

N1-ST-Q3, High-Pressure Coolant Injection Pump and Check Valve Operability Test,

Revision 01300

N1-TSP-201-001, Integrated Leak Rate Test of Primary Containment Type A Test, Revision

00600

N2-CSP-GEN-D100, Reactor Water/Auxiliary Water Chemistry Surveillance, Revision 00601

N2-ISP-LDS-Q010, Reactor Building General Area Temperature Instrument Channel Functional

Test, Revision 00103

N22-CSP-W@101, Weekly Conductivity Monitor Channel Check, Revision 1

S-CAD-CHE-101, Chemistry Sample Conduct, Revision 0100

Condition Reports

CR-2013-002788

CR-2013-002637

Drawings

C-18013-C, Reactor Building Heating and Ventilation System, Revision 33

C-18014-C, Reactor Containment (Drywell and Torus) Inert Gas N2 Purge and Fill Drywell

Cooling System, Revision 58

Work Orders

WO C91214116

WO C92182070

Attachment

A-11

Miscellaneous

NUREG-1493, Performance-Based Containment Leak Test Program, September 1995

Section 1EP4: Emergency Action Level and Emergency Plan Changes

Procedures

EPIP-EPP-01, Classification of Emergency Conditions at Unit 1, Revision 23

EPIP-EPP-02, Classification of Emergency Conditions at Unit 2, Revision 22

EPMP-EPP-0101, Unit 1 Emergency Classification Technical Bases, Revision 01700

EPMP-EPP-0102, Unit 2 Emergency Classification Technical Bases, Revision 01900

Section 1EP6: Drill Evaluation

Procedure

EPIP-EPP-01, Classification of Emergency Conditions at Unit 1, Revision 02000

Section 2RS1: Radiological Hazard Assessment and Exposure Controls

Procedures

CNG-TR-1.01-1025, Radiation Protection Technician Training Program, Revision 00100

GAP-RPP-08, Control of High Locked High and Very High Radiation Areas, Revision 16

S-RAP-RPP-0103, Posting and Barricading Radiological Areas, Revision 02800

S-RAP-RPP-0201, Radiation Work Permit Initiation, Preparation, Control and Use,

Revision 02300

S-RAP-RPP-0801, High Locked High and Very High Radiation Area Monitoring and Control,

Revision 03000

S-RPIP-3.0, Radiological Surveys, Revision 01900

Condition Reports

CR-2013-002520

CR-2013-002781

CR-2013-003098

Audits, Self Assessments, and Surveillances

Q&PA Assessment Report 13-010, Assess Station Preparedness for Managing and Executing

N1R23

SA-2013-000005, Snapshot Assessment of 2012 4th Quarter Dose and Dose Rate Alarms

SA-2013-000034, Snapshot Assessment of Radiation Protection Job Hazard Analysis Process

Usage

Miscellaneous

BRAC Survey Trends in Discharge Piping Dose Rates, Unit 1, 1984 to 2013

BRAC Survey Trends in Recirc Suction Piping Dose Rates, Unit 1, 1984 to 2013

High Radiation Area/Locked High Radiation Area Gate Door Checklist, Unit 1, April 20, 2013

Personnel Qualification Form Verification, Employee Badge 38016, April 8, 2013

Personnel Qualification Form Verification, Employee Badge 38359, April 1, 2013

Personnel Qualification Form Verification, Employee Badge 4127, April 8, 2013

Personnel Qualification Form Verification, Employee Badge 4169, April 1, 2013

Personnel Qualification Form Verification, Employee Badge 4196, March 29, 2013

Attachment

A-12

Personnel Qualification Form Verification, Employee Badge 54337, February 25, 2013

RWP 113330H, RB 261 Reactor Water Cleanup Valve Work

RWP 113802H, Drywell Under-Vessel Work

RWP 113806H, Drywell In-Service Inspection

RWP 113810, Drywell General Scaffolding Activities

RWP 113815, RB 261 FAC In-Service Inspection

RWP 113890A, RB 340 Reactor Disassembly and Reassembly

RWP 113890B, RB 340 Underwater Work on Refuel Floor

RWP 113890E, RB 340 Reactor Cavity and Equipment Storage Pit Decon

RWP 113891, Spent Fuel Pool Gate Repair

Section 2RS2: Occupational ALARA Planning and Controls

Procedures

CNG-RP-1.01-1001, Station ALARA Committee, Revision 00000

CNG-RP-1.01-2003, Operational ALARA Planning and Controls, Revision 00000

N1-OP-34, Refueling Procedure (Includes Primary Chemistry Controls), Revision 03000

S-RAP-ALA-0101, Temporary Shielding, Revision 10

S-RAP-ALA-0102, ALARA Reviews, Revision 01500

Condition Reports

CR-2013-002267

CR-2013-003168

Self Assessment

SA-2012-000283, 4th Quarter 2012 ALARA Committee Effectiveness Review

Miscellaneous

5-Year Collective Radiation Exposure Reduction Plan, 2012 to 2016

ALARA Plan 2013-1-002, Drywell Under-Vessel Activities and Associated Activities N1R22,

April 10, 2013

ALARA Plan 2013-1-004, Drywell Operations and LLRT/ILRT Activities, April 10, 2013

ALARA Plan 2013-1-006, Drywell ISI Activities, April 10, 2013

ALARA Plan 2013-1-007, Recirc Pump Seals Replacement and Motor PMs (Numbers 11, 13 and

15), April 10, 2013

ALARA Plan 2013-1-010, Drywell Scaffold Activities, April 10, 2013

ALARA Plan 2013-1-014, Drywell Emergency Relief Valve and Pilot Valve Work Activities,

April 10, 2013

ALARA Plan 2013-1-024, Main Steam Isolation Valve 01-02 Stem Replacement Actuator

Remove/Replace and Testing, April 10, 2013

ALARA Plan 2013-1-029, Balance of Plant FAC Activities in RWCU HX Room and Valve Aisles,

April 10, 2013

ALARA Plan 2013-1-030, Refuel Floor Activities, dated April 10, 2013

ALARA Plan 2013-1-031, RWCU Miscellaneous Maintenance, PM, ST, Operations RFO 22,

April 10, 2013

ALARA Work In-Progress Review, 2013-1-006, Drywell ISI Activities, April 21, 2013

ALARA Work In-Progress Review, 2013-1-007, Recirc Pump Seals Replacement and Motor PMs,

April 22, 2013

ALARA Work In-Progress Review, 2013-1-010, Drywell Scaffold Activities, April 20, 2013

Attachment

A-13

ALARA Work In-Progress Review, 2013-1-011, Drywell Insulation, April 22, 2013

ALARA Work In-Progress Review, 2013-1-014, Drywell Emergency Relief Valve and Pilot Valve

Work Activities, April 22, 2013

ALARA Work In-Progress Review, 2013-1-024, Main Steam Isolation Valve 01-02 Stem

Replacement Actuator Remove/Replace and Testing, April 22, 2013

ALARA Work In-Progress Review, 2013-1-029, Balance of Plant FAC Activities in RWCU HX

Room and Valve Aisles, April 18, 2013

ALARA Work In-Progress Review, 2013-1-030, Refuel Floor Activities, April 20, 2013

Unit 1 Radiation Protection Pre-Outage Report, dated April 15, 2013

Section 2RS3: In-Plant Airborne Radioactivity Control and Mitigation

Procedures

GAP-RPP-04, Respiratory Protection Program, Revision 11

N1-RTP-76, Operation and Calibration of the Eberline PING-1A PING-1AMT Particulate Iodine

Noble Gas Monitor, Revision 02

S-RAP-RPP-0402, Selection and Issuance of Radiological Respiratory Protection Equipment,

Revision 12

S-RPIP-4.2, Respiratory Protection Quality Assurance Control Program, Revision 00200

S-RPIP-4.4, Maintenance Inspection and Testing of Respiratory Protection Equipment,

Revision 00700

S-RPIP-4.5, Use of Respiratory Protection Equipment, Revision 09

S-RPIP-6.0, Control and Use of HEPA Vacuum Cleaners and Portable HEPA Ventilation Units,

Revision 00300

Condition Reports

CR-2013-002816

CR-2013-002947

Self Assessment

SA-2011-000164, Radiological Respiratory Protection Program, November 18, 2011

Miscellaneous

Air Sample Unit 1 RB 340 Edge of Cavity, April 15, 2013, 5:43 a.m.

Air Sample Unit 1 RB 340 Edge of Cavity, April 15, 2013, 7:14 a.m.

Air Sample Unit 1 RB 340 Refuel Floor during Silver Dollar Installation, April 15, 2013, 9:20 p.m.

Air Sample Unit 1 RB 340 Refuel Floor during Stud Removal, April 17, 2013, 12:20 p.m.

HEPA Ventilation Log, dated April 23, 2013

Unit 1 System Health Report for 1st Quarter Control Room Ventilation, dated April 10, 2013

Unit 1 System Health Report for 1st Quarter RB Ventilation, dated April 10, 2013

Vacuum Cleaner Issue Log, dated April 23, 2013

Section 2RS4: Occupational Dose Assessment

Procedures

CNG-RP-1.01-2002 Effective Dose Equivalent - External, Revision 00000

CNG-RP-1.01-3002, Sampling and Analysis for 10 CFR 61 Waste Classification, Revision 00000

GAP-RPP-07, Internal and External Dosimetry Program, Revision 02100

S-RAP-ALA-0103, Dosimetry and Radiological Engineering Evaluations, Revision 00900

S-RPIP-4.6, DAC Hour Tracking and Estimating Internal Exposure, Revision 00500

Attachment

A-14

S-RPIP-5.5, Processing and Evaluating Personnel Contamination, Revision 01800

S-RPIP-5.7, Bioassay and Internal Dose Assessment, Revision 00900

S-RPIP-5.20, Dosimetry Program Quality Assurance, Revision 00800

S-RPIP-5.25, Exposure Evaluation Reports, Revision 01000

Condition Reports

CR-2013-002474

CR-2013-002678

CR-2013-002974

CR-2013-003247

CR-2013-003374

CR-2013-003350

CR-2013-003413

Miscellaneous

Oak Ridge Associated University E-mail Y. McCormick to A. Moisan RE: REIRS Data Verification,

dated April 1, 2013

Sentinel Report on Personnel with Dose Greater Than 400 mrem, dated April 22, 2013

S-RPIP-5.5 Attachment 1 Contamination Occurrence Report Number 1-13-RFO-003, dated

April 24, 2013

Section 2RS7: Radiological Environmental Monitoring Program

Procedures

CNG-EV-1.01-1000, Radiological Environmental Monitoring Program, Revision 001000

NLAP-ENV-400, Radiological Environmental Monitoring Program Land Use Census,

Inter-laboratory Comparison Program and Reporting, Revision 00.00

S-ENVSP-3, Radiological Sample Collection, Processing, and Shipment Land Use Census

Quality Control (Vendor Procedure), Revision 06.00

S-ENVSP-3.1, Milk Animal Census and Milk Sample Collection, Revision 01.00

S-ENVSP-3.2, Garden/Irrigation Census and Food Product (Vegetation and Irrigation Crop)

Sample Collection, Revision 02.00

S-ENVSP-3.3, Nearest Meat Animal Census and Meat, Poultry, and Egg Sample Collection,

Revision 01.00

S-ENVSP-3.4, Soil Sample Collection, Revision 01.00

S-ENVSP-3.5, Fish Sample Collection, Revision 01.00

S-ENVSP-3.6, Shoreline Sediment and Cladophora Sample Collection, Revision 01.00

S-ENVSP-3.7, Nearest Residence Census, Revision 00.00

S-ENVSP-4.1, TLD/OSL Preparation, Collection and Analysis, Revision 01400.00

S-ENVSP-4.2, Environmental Air Monitoring Sample Collection, Revision 01001.00

S-ENVSP-4.3, Environmental Air Monitoring Station Inspection and Maintenance,

Revision 00600.00

S-ENVSP-4.4, Environmental Surface Water Sample Collection and Compositing,

Revision 00900.00

S-ENVSP-12, Environmental Surveillance Quality Assurance/Quality Control Program,

Revision 001100.00

S-ENVSP-15, Sampling and Analysis for Unmonitored Pathways, Revision 01300.00

S-ENVSP-16, Sampling and Analysis of Monitoring Wells, Revision 00500.00

S-ENVSP-18, Environmental Data Review, Revision 01000.00

S-IPM-MET-001, Meteorological Monitoring System Equipment Check, Revision 00200.00

Attachment

A-15

S-IPM-MET-201, Dew Point Calibration, Revision 00100.00

S-IPM-MET-301, Barometric Pressure Calibration, Revision 03.00

S-IPM-MET-401, Precipitation Gauge Calibration, Revision 02.00

S-IPM-MET-601, Main Meteorological Tower 30 Foot Wind Speed and Direction Calibration,

Revision 00100.00

S-IPM-MET-602, Main Meteorological Tower 100 Foot Wind Speed and Direction Calibration,

Revision 00400.00

S-IPM-MET-603, Main Meteorological Tower 200 Foot Wind Speed and Direction Calibration,

Revision 00100.00

S-IPM-MET-611, Backup Meteorological Tower Wind Speed and Direction Calibration,

Revision 00200.00

S-IPM-MET-621, Inland Meteorological Tower Wind Speed and Direction Calibration,

Revision 00100.00

S-IPM-MET-701, Temperature and Delta Temperature Instrument Calibration,

Revision 00200.00

S-MET-ENV-01, Maintenance of Meteorological Monitoring Program, Revision 00100.00

S-MET-ENV-0002, Meteorological Data Verification and Edit, Revision 00600.00

S-MET-ENV-0003, Meteorological Monitoring Program Quality Assurance Quality Control,

Revision 00600.00

Condition Reports

CR-2012-000632 CR-2012-005817 CR-2012-010132

CR-2012-000664 CR-2012-006057 CR-2013-000603

CR-2012-000734 CR-2012-007114 CR-2013-001001

CR-2012-001143 CR-2012-007684

CR-2012-001488 CR-2012-009863

Work Orders

WO C91660878

WO C91875097

Audits, Self Assessments, and Surveillances

DTE Energy NAQA-12-0036, Audit 12-006 of Environmental Dosimetry Company, July 3, 2012

Entergy CR-LO-JAFLO-2012-00045, Radiological Environmental Monitoring Program Focused

Self Assessment, February 20 to 27, 2013

NUPIC Audit 22873, GEL Laboratories, LLC, Analytical Laboratory Services, December 13, 2011

Miscellaneous

2011 Annual Report, Meteorological Monitoring Program, Murray and Trettel, Inc., Palatine, IL

2012 Annual Quality Assurance Status Report, Environmental Dosimetry Company, dated

March 13, 2013

2012 Inter-laboratory Comparison Report, Eckert and Zeigler, dated March 29, 2013

2012 Land Use Census Summary Report, dated October 25, 2012

DVP-04.01, Environmental Laboratory Quality Assurance/Quality Control Program, Revision 4

EN-CY-102, Laboratory Analytical Quality Control, Revision 4

James A. FitzPatrick Environmental Laboratory Quality Assurance Report, January to

December 2011

Licensee Event Number 48901, Power Lost to Meteorological Instrumentation, dated April 9, 2013

Quality Assurance Topical Report, dated December 11, 2011

Attachment

A-16

Radiological Environmental Operating Report January to December, 2012, dated May 15, 2013

Radiological Engineering Evaluation Number C-99-011, Revision 7, 10 CFR 50.75(g) Record -

Unit 1 TB Roof Replacement, dated September 7, 2012

Radiological Engineering Evaluation Number C-99-011, Revision 8, 10 CFR 50.75(g) Record -

Elevated Tritium Concentration in Screen House In-Leakage, dated January 27, 2013

S-ENVSP-4.4 Attachment 5A L/S 7523 Sample Pump Control Setting Determination, Serial

Number L03004172, NRG Oswego Steam Station, dated August 14, 2009

S-ENVSP-4.4, Attachment 5A, L/S 7523 Sample Pump Control Setting Determination, Serial

Number L04004587, Unit 1 Intake Canal, dated April 20, 2009

S-ENVSP-4.4, Attachment 5A, L/S 7523 Sample Pump Control Setting Determination, Serial

Number L04004590, Unit 1 Intake Canal, dated April 20, 2009

Tektronix Certificate of Calibration 6776890, American Meter Mass Flow Meter Number 10429,

dated November 16, 2012

Tektronix Certificate of Calibration 6104009, American Meter Mass Flow Meter Number 10436,

dated April 20, 2012

Tektronix Certificate of Calibration 6780305, American Meter Mass Flow Meter Number 10458,

dated November 17, 2012

Tektronix Certificate of Calibration 6114558, American Meter Mass Flow Meter Number 10870,

dated April 23, 2012

Tektronix Certificate of Calibration 6380789, American Meter Mass Flow Meter Number 10899,

dated July 18, 2012

Unit 1 ODCM, Revision 34

Unit 1 Radioactive Effluent Release Report, January to December 2012, dated May 1, 2013

Unit 2 ODCM, Revision 35

Unit 2 UFSAR Chapter 2.3, Meteorology, Revision 19, October 2010

Section 4OA1: Performance Indicator Verification

Procedures

N2-CSP-GEN-D100, Reactor Water/Auxiliary Water Chemistry Surveillance, Revision 00601

N22-CSP-W@101, Weekly conductivity Monitor Channel Check, Revision 1

S-CAD-CHE-101, Chemistry Sample Conduct, Revision 01100

Miscellaneous

Nuclear Energy Institute 99-02, Regulatory Assessment Performance Indicator Guideline,

Revision 6

Section 4OA2: Problem Identification and Resolution

Procedures

CENG-AM-1.01-1005, Engineering Role and Responsibilities/Expectations, Revision 00303

CNG-CA-1.01-1004, Root Cause Analysis, Revision 00802

CNG-CA-2.01-1000, Self-Assessment and Benchmarking Process, Revision 00700

CNG-MN-4.01-1001, Work Order Execution and Closure Process, Revision 00401

CNG-MN-1.01-1000, Conduct of Maintenance, Revision 00200

N2-EMP-GEN-673, 24/48 VDC and 125 VDC Batteries - Cell and Connector Replacement,

Revision 00400

NPAP-INV-220, Storage and Handling of Material, Revision 01001

Nine Mile Point Station Policy Number 22, Work Document Quality, Revision 0

Attachment

A-17

Procedure Review Briefing Sheet CNG-HU-1.01-1001 HU Tools and Verification Process

Understanding Human Behavior and Error, Human Reliability Associates, David Embrey

Condition Reports

CR-1997-001696 CR-2012-000060 CR-2012-009469

CR-2001-005920 CR-2012-001137 CR-2012-010774

CR-2005-003461 CR-2012-001138 CR-2012-010907

CR-2007-007514 CR-2012-001139 CR-2013-001159

CR-2010-001220 CR-2012-001315 CR-2013-002102

CR-2010-001987 CR-2012-001316 CR-2013-002360

CR-2010-003899 CR-2012-002716 CR-2013-002443

CR-2010-007337 CR-2012-003724 CR-2013-003207

CR-2011-005737 CR-2012-004600 CR-2013-003357

CR-2011-007171 CR-2012-005362 CR-2013-005074

CR-2011-007269 CR-2012-005365 CR-2013-005117

CR-2011-007655 CR-2012-006030 CR-2013-005228

CR-2011-009896 CR-2012-006242 CR-2013-005235

CR-2011-010906 CR-2012-006823 CR-2013-005245

CR-2011-010953 CR-2012-007085

CR-2011-011006 CR-2012-007765

Drawings

3.N2.1-E21.1, One Line Diagram 125 VDC Control Bus, Revision 14

EE-1CA, One Line Diagram Emergency and Vital Bus Power Distribution Unit 2, Revision 14

EE-1CM, 125 VDC One Line Diagram Emergency Switchgear 2BYS*SWG002A, Revision 19

EE-1CN, 125 VDC One Line Diagram Emergency Switchgear 2BYS*SWG002B, Revision 17

EE-MO1F, Plant Master One Line Diagram Emergency and Normal 125V and 24/48VDC Unit 2,

Revision 8

Work Orders

WO C92017475

WO C92036878

Miscellaneous

CR Search for RCS*MOV18, Excessive Unidentified Leakage, and TS Required Shutdown for

January 1, 2000, until April 25, 2013

Design Engineering Request NM-2001-5894

Equipment Reliability Return to Excellence Plan

Equivalency Evaluation Number 00230 for RCS*MOV 10A&B and RCS*MOV 18A&B, dated

April 4, 2002

GE SIL No. 620, BWR 5 and 6 Reactor Recirculation System Pump Discharge Gate Valve

N2-ESP-BYS-Q767, Quarterly Battery Surveillance Test, completed on August 16 and 31, 2012;

February 11, March 7, and May 28, 2013

N2-ESP-BYS-R685, Divisions I, II, and III Battery Modified Profile Test, completed on April 4

and 10, 2010; April 16, July 25, and November 28, 2012

Root Cause Analysis, Cross-Cutting Theme Exists in the Aspect of Human Performance,

Resources, Documentation H.2(c) dated January 18, 2013

Root Cause Analysis, Unit 1 SCRAM due to Turbine Trip on May 2, 2011, dated

September 16, 2011

Attachment

A-18

Timeline of RCS*MOV 18A Problems

Unit 1 DEP System Health Report, 1st and 2nd Quarters 2013

Unit 2 DEP System Health Report, 1st and 2nd Quarters 2013

Valve Packing Data Sheet for RCS*MOV 10A and B

Valve Packing Data Sheet for RCS*MOV 18A and B

Vendor Manuals

35.40, Specifications Nuclear Class 1E Flooded Batteries GNB, dated August 2002

RS-1476, Stationary Battery and Vented Cell Installation and Operating Instructions C&D

Technologies, dated 2009

Calculation

EC-145, Verification of Adequacy of Division III Battery 2BYS*BAT2C, Revision 2

Section 4OA3: Follow-up of Events and Notices of Enforcement Discretion

Procedures

N1-OP-47A, 125 VDC Power System, Revision 02500

N1-SOP-47A.1, Loss of DC, Revision 00101

N1-SOP-6.1, Loss of SFP/RX Cavity Level/Decay Heat Removal, Revision 00501

N1-ST-R2, LOCA and EDG Simulated Auto Initiation Test, Revision 03201

N2-EMP-GEN-609, General Small Motor Maintenance, Revision 06

NIP-OUT-01, Shutdown Safety, Revision 03700

Condition Reports

CR-2013-001633

CR-2013-002916

CR-2013-002926

CR-2013-002958

CR-2013-002998

Miscellaneous

ACE for CR-2013-001633

CENG Safety Stand Down for April 16, 2013, Loss of Battery Bus 12 Event

Control Room Operator Logs for Tuesday, April 16, 2013

E191, NMPNS Specification for Safety-Related Motor Repairs, Revision 0

Outage Control Center Logs for Tuesday, April 16, 2013

PM Template for Small and Intermediate HP Motors

Unit 1 Station Alarm Log for Tuesday, April 16, 2013

Work Control Center Turnover Sheet for April 16, 2013, Days to Night

Attachment

A-19

LIST OF ACRONYMS

10 CFR Title 10 of the Code of Federal Regulations

AC alternating current

ADAMS Agencywide Documents Access and Management System

ALARA as low as reasonably achievable

ASME American Society of Mechanical Engineers

BWR boiling-water reactor

CAP corrective action program

CENG Constellation Energy Nuclear Group, LLC

DC direct current

ECCS emergency core cooling system

ECP engineering change package

EDG emergency diesel generator

ERV electro-matic relief valve

FA fire area

FAC flow accelerated corrosion

FCV flow control valve

HPCS high-pressure core spray

I&C instrumentation and control

IEEE Institute of Electrical and Electronics Engineers

IMC Inspection Manual Chapter

ISI inservice inspection

kV kilovolt

LER licensee event report

LOCA loss of coolant accident

LOOP loss of offsite power

NDE nondestructive examination

NCV non-cited violation

NMPNS Nine Mile Point Nuclear Station, LLC

NRC Nuclear Regulatory Commission

ODCM offsite dose calculation manual

psig pounds per square inch gauge

RB reactor building

RCIC reactor core isolation cooling

RCS reactor coolant system

REMP radiological environmental monitoring program

RG regulatory guide

RHR residual heat removal

RPT radiation protection technician

RPV reactor pressure vessel

RWCU reactor water cleanup

RWP radiation work permit

SDC shutdown cooling

SDP significance determination process

SFP spent fuel pool

SSC structure, system, and component

Enclosure

A-20

ST surveillance testing

TLD thermo luminescent dosimeter

TS technical specification

UFSAR Updated Final Safety Analysis Report

UT ultrasonic testing

VDC volts direct current

Attachment