IR 05000220/2022001

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Integrated Inspection Report 05000220/2022001 and 05000410/2022001
ML22119A018
Person / Time
Site: Nine Mile Point  
Issue date: 04/29/2022
From: Erin Carfang
Division of Operating Reactors
To: Rhoades D
Constellation Energy Generation, Constellation Nuclear
Carfang E
References
IR 2022001
Download: ML22119A018 (21)


Text

April 29, 2022

SUBJECT:

NINE MILE POINT NUCLEAR STATION, UNITS 1 AND 2 - INTEGRATED INSPECTION REPORT 05000220/2022001 AND 05000410/2022001

Dear Mr. Rhoades:

On March 31, 2022, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Nine Mile Point Nuclear Station, Units 1 and 2. On April 21, 2022, the NRC inspectors discussed the results of this inspection with Mr. Peter Orphanos, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.

No findings or violations of more than minor significance were identified during this inspection.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Erin E. Carfang, Chief Projects Branch 1 Division of Operating Reactor Safety

Docket Nos. 05000220 and 05000410 License Nos. DPR-63 and NPF-69

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000220 and 05000410

License Numbers:

DPR-63 and NPF-69

Report Numbers:

05000220/2022001 and 05000410/2022001

Enterprise Identifier: I-2022-001-0049

Licensee:

Constellation Energy Generation, LLC

Facility:

Nine Mile Point Nuclear Station, Units 1 and 2

Location:

Oswego, NY

Inspection Dates:

January 1, 2022 to March 31, 2022

Inspectors:

G. Stock, Senior Resident Inspector

C. Kline, Resident Inspector

B. Sienel, Resident Inspector

N. Floyd, Senior Reactor Inspector

S. Haney, Senior Project Engineer

C. Hobbs, Reactor Inspector

S. Wilson, Senior Health Physicist

Approved By:

Erin E. Carfang, Chief

Projects Branch 1

Division of Operating Reactor Safety

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Nine Mile Point Nuclear Station, Units 1 and 2, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

None.

PLANT STATUS

Unit 1 operated at or near rated thermal power for the entire inspection period.

Unit 2 began the inspection period at rated thermal power. On January 7, 2022, the unit was downpowered to 78 percent to perform planned control rod channel interference testing and a control rod pattern adjustment, and returned to rated thermal power on January 8, 2022.

On January 28, 2022, the unit began end-of-cycle coastdown. On February 11, 2022, the unit was downpowered to 85 percent to avoid a known oscillation region during end-of-cycle coastdown. On March 7, 2022, the unit was shut down for a planned refueling outage. Startup was commenced on March 25, 2022, and rated thermal power was reached on March 29, 2022. Later that day, the unit was downpowered to 80 percent for a planned rod pattern adjustment. During the downpower, a main turbine control valve malfunction required an additional downpower to 60 percent. The unit returned to rated thermal power on March 31, 2022, and remained at or near rated thermal power for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed activities described in IMC 2515, Appendix D, Plant Status, conducted routine reviews using IP 71152, Problem Identification and Resolution, observed risk-significant activities, and completed on-site portions of IPs. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

On February 1, 2022, the operating license for Nine Mile Point Nuclear Station, held by Exelon Generation Company, LLC, was transferred to Constellation Energy Generation, LLC (Constellation). While some or all of the inspections documented in this report were performed while the license was held by Exelon Generation Company, LLC, this report will refer to the licensee as Constellation throughout.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Impending Severe Weather Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated the adequacy of the overall preparations to protect risk-significant systems due to a winter storm warning on March 11, 2022.

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (7 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Unit 2 reactor core isolation cooling system on January 26, 2022
(2) Unit 1 reactor building closed loop cooling system on February 7, 2022
(3) Unit 2 'C' residual heat removal system on February 7, 2022
(4) Unit 2 Division II emergency diesel generator on February 22, 2022
(5) Unit 2 'B' residual heat removal system in shutdown cooling on March 8, 2022
(6) Unit 2 Division I emergency diesel generator on March 10, 2022
(7) Unit 2 'A' spent fuel pool cooling system on March 15, 2022

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (9 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:

(1) Unit 2 radwaste building 261/265, condensate storage building, fire area 55, on February 1, 2022
(2) Unit 2 reactor building 289, fire areas 34 and 35, on February 10, 2022
(3) Unit 2 reactor building 240 north, fire area 1, on February 14, 2022
(4) Unit 1 turbine building 261' west, fire area 5, on February 17, 2022
(5) Unit 2 reactor building 175' north, fire area 1, on February 28, 2022
(6) Unit 2 reactor building, primary containment steam tunnel, fire area 50, on March 7, 2022
(7) Unit 2 turbine building, condenser, fire area 50, on March 7, 2022
(8) Unit 2 turbine building, feedwater heater bays, fire area 50, on March 9, 2022
(9) Unit 2 reactor building, drywell, fire area 5, on March 16, 2022

71111.06 - Flood Protection Measures

Inspection Activities - Internal Flooding (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated internal flooding mitigation protections in the Unit 1 cable spreading room on February 28, 2022.

71111.07A - Heat Exchanger/Sink Performance

Annual Review (IP Section 03.01) (1 Sample)

The inspectors evaluated readiness and performance of:

(1) Unit 2 'B' residual heat removal heat exchanger

71111.08G - Inservice Inspection Activities (BWR)

BWR Inservice Inspection Activities Sample - Nondestructive Examination and Welding

Activities (IP Section 03.01)

(1) The inspectors verified that the reactor coolant system boundary, reactor vessel internals, risk-significant piping system boundaries, and containment boundary are appropriately monitored for degradation, and that repairs and replacements were appropriately fabricated, examined and accepted by reviewing the following activities from March 7 to March 17, 2022:

==2R18 -ISI-UT-002 / -003).

  • ==

Visual examinations of the containment, including accessible portions of the drywell and suppression chamber metal liner (Work Order [WO] C93672957)

  • Welding activities associated with the modification of the instrument air check valve, 2IAS*V450, under engineering change ECP-21-000088 (Work Order

[WO] 93782709). This included liquid penetrant testing of two pipe-to-valve welds, FW-03 and FW-04 (NDE Report BOP-PT-22-004).

  • Flaw evaluation of the embedded reflector identified during the spring 2020 refueling outage using automated phased array UT on the N2J reactor recirculation nozzle to safe-end dissimilar metal weld (NDE Report N2R17-APR-06). The flaw was determined to be acceptable for continued service.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (2 Samples)

(1) The inspectors observed Unit 1 operations personnel during control rod exercising operability testing on March 5, 2022.
(2) The inspectors observed Unit 2 operations personnel during the plant shutdown for refueling outage N2R18 on March 6, 2022.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (2 Samples)

(1) The inspectors observed a Unit 2 simulator evaluation that included an instrument air compressor failure, reactor core isolation cooling system inoperability, and a small loss of coolant accident with additional failures that required the depressurization of the reactor on January 25, 2022.
(2) The inspectors observed a Unit 1 simulator evaluation that included the inadvertent opening of an electromatic relief valve, a loss of offsite power, an emergency diesel generator failure to start, and a steam leak in the drywell on February 2, 2022.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (1 Sample)

The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended function:

(1) Unit 2 Division I emergency diesel generator jacket water pump

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (9 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1) Unit 2 elevated risk during planned 'B' residual heat removal pump maintenance on January 4, 2022
(2) Unit 2 elevated risk during emergent work on the Division I emergency diesel generator starting air system on January 20, 2022
(3) Unit 1 elevated risk during emergent work on the 'C' instrument air compressor on February 16, 2022
(4) Unit 2 elevated risk during planned Division I emergency diesel generator maintenance on February 22, 2022
(5) Unit 2 elevated risk during emergent work on the 'B' service water pump on March 2, 2022
(6) Unit 2 elevated risk during a planned 115-kilovolt Line 5 outage on March 6, 2022
(7) Unit 2 elevated risk during a planned reactor cavity flood-up on March 8, 2022
(8) Unit 2 elevated risk during planned maintenance on SWP*MOV66B, cooling water to Division II emergency diesel generator, on March 10-12, 2022
(9) Unit 2 elevated risk during a planned reactor cavity draindown on March 22, 2022

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (9 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:

(1) Unit 2 Division I emergency diesel generator slow start on January 3, 2022
(2) Unit 2 Division I emergency diesel generator starting air compressor 'B' failure on January 18, 2022
(3) Unit 2 Division I emergency diesel generator emergency start solenoid valve air leaks on January 20, 2022
(4) Unit 1 safety relief valve elevated discharge temperature indications on February 1, 2022
(5) Unit 1 emergency diesel generator 103 starting flywheel chipped tooth on February 15, 2022
(6) Unit 1 containment spray raw water 122 rate set valve unable to operate on February 24, 2022
(7) Unit 1 core spray topping pump 111 pump-bearing oil leak on March 2, 2022
(8) Unit 2 Division III diesel under voltage relay failure to reset after testing on March 4, 2022
(9) Unit 2 main steam isolation valve slow fast closure times on March 7, 2022

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (3 Samples)

The inspectors evaluated the following temporary or permanent modifications:

(1) Permanent Modification: ECP-21-000437, Unit 2 Division II Emergency Diesel Generator Governor Booster
(2) Permanent Modification: ECP-21-000454, Unit 2 Digital Electro-Hydraulic Control (DEHC) Low Pass Filter Modification
(3) Permanent Modification: ECP-21-000088, Unit 2 PCIV [primary containment isolation valve] Supply Nitrogen Line Primary Containment Inboard Isolation Re-Design

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the following post-maintenance testing activities to verify system operability and/or functionality:

(1) Unit 2 Division I emergency diesel generator jacket water pump following replacement on February 23, 2022
(2) Unit 2 'B' service water pump following a failure to start on March 2, 2022
(3) Unit 2 Division II emergency diesel generator following governor oil booster installation on March 21, 2022
(4) Unit 2 'B' residual heat removal system following heat exchanger inspection on March 25, 2022
(5) Unit 2 drywell nitrogen supply system following solenoid operated valve replacement on March 28, 2022

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated Unit 2 refueling outage N2R18 from March 6 to March 27, 2022.

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance testing activities to verify system operability and/or functionality:

Surveillance Tests (other) (IP Section 03.01) (8 Samples)

(1) N1-ST-M4A, Emergency Diesel Generator 102 and PB 102 Operability Test, on January 24, 2022
(2) N2-OSP-CSL-Q@002, LPCS [low pressure core spray] Pump and Valve Operability and System Integrity Test, on February 28, 2022
(3) N1-ST-Q1A, Core Spray 111 Pump, Valve and Shutdown Cooling Water Seal Check Valve Operability Test, on March 1, 2022
(4) N2-OSP-MSS-CS001, Main Steam Isolation Valve Operability Test, on March 7, 2022
(5) N2-OSP-RHS-R001, Division II ECCS [emergency core cooling system] Functional Test, on March 9, 2022
(6) N2-OSP-SLS-R001, Standby Liquid Control Manual Initiate Actuation and ASME XI Pressure Test, on March 16, 2022
(7) N2-OSP-ADS-R002, ADS [automatic depressurization system] Functional Test and Remote Shutdown System Test, on March 19, 2022
(8) N2-OSP-EGS-R001, Diesel Generator ECCS Start and Load Reject Division II, on March 20, 2022

Inservice Testing (IP Section 03.01) (2 Samples)

(1) N2-OSP-ICS-Q@002, Reactor Core Isolation Cooling Pump and Valve Operability Test and System Integrity Test and ASME XI Functional Test and Analysis, on February 10, 2022
(2) N2-ISP-RRC-R001, ARI [alternate rod insertion] Function of RRCS [redundant reactivity control system], on March 7, 2022

Containment Isolation Valve Testing (IP Section 03.01) (2 Samples)

(1) N2-OSP-MSS-003, Unit 2 Main Steam Isolation Valve Leak Rate Test, on March 7, 2022
(2) N2-OSP-MSS-004, Unit 2 Main Steam Isolation Valve Leak Rate Test (Reactor Vessel Head Removed), on March 25,

RADIATION SAFETY

71124.01 - Radiological Hazard Assessment and Exposure Controls

Radiological Hazard Assessment (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated how the licensee identifies the magnitude and extent of radiation levels and the concentrations and quantities of radioactive materials and how Constellation assesses radiological hazards.

Instructions to Workers (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated how the licensee instructs workers on plant-related radiological hazards and the radiation protection requirements intended to protect workers from those hazards.

Contamination and Radioactive Material Control (IP Section 03.03) (2 Samples)

The inspectors observed/evaluated the following licensee processes for monitoring and controlling contamination and radioactive material:

(1) Workers exiting the Unit 2 radiologically controlled area during refueling outage N2R18
(2) Licensee surveys of contaminated equipment on the refuel floor during refueling outage N2R18

Radiological Hazards Control and Work Coverage (IP Section 03.04) (5 Samples)

The inspectors evaluated the licensee's control of radiological hazards for the following radiological work:

(1) Unit 2 outage refuel floor activities, low power range monitor exchange, and supporting activities
(2) Unit 2 in-vessel inspection and supporting activities
(3) Unit 2 refuel floor equipment decontamination activities
(4) Unit 2 drywell feedwater nozzle inspection activities
(5) Unit 2 safety relief valve maintenance in the drywell

High Radiation Area and Very High Radiation Area Controls (IP Section 03.05) (2 Samples)

The inspectors evaluated licensee controls of the following High Radiation Areas and Very High Radiation Areas:

(1) High Radiation Area in the Unit 2 reactor building valve pit, 196' elevation
(2) Locked High Radiation Areas in the Unit 2 drywell

Radiation Worker Performance and Radiation Protection Technician Proficiency (IP Section 03.06) (1 Sample)

(1) The inspectors evaluated radiation worker and radiation protection technician performance as it pertains to radiation protection requirements.

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 02.01)===

(1) Unit 1 (January 1, 2021 through December 31, 2021)
(2) Unit 2 (January 1, 2021 through December 31, 2021)

IE03: Unplanned Power Changes per 7000 Critical Hours Sample (IP Section 02.02) (2 Samples)

(1) Unit 1 (January 1, 2021 through December 31, 2021)
(2) Unit 2 (January 1, 2021 through December 31, 2021)

IE04: Unplanned Scrams with Complications (USwC) Sample (IP Section 02.03) (2 Samples)

(1) Unit 1 (January 1, 2021 through December 31, 2021)
(2) Unit 2 (January 1, 2021 through December 31, 2021)

===71152A - Annual Follow-up Problem Identification and Resolution

Annual Follow-up of Selected Issues (Section 03.03)===

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) IR 04436618 - Nine Mile Point Control Rod Blade Technical Evaluation

INSPECTION RESULTS

Observation: Nine Mile Point Control Rod Blade Technical Evaluation 71152A On November 23, 2020, General Electric Hitachi (GEH) released Safety Communication 20-06 (SC 20-06) Revision 0, describing the discovery that Boron 10 (B-10) depletion had been underpredicted in the top 6-inch node of the neutron absorber section of control rod blades currently in use in boiling water reactors in the United States. Nine Mile Point Nuclear Station was on the list of plants affected by this issue. In Revision 0 of the Safety Communication, the population of control rod blades affected was restricted to Original Equipment Manufacturer (OEM) series D-100 control rod blades, still in operation from the 1970s and 1980s. On February 26, 2021, GEH issued Revision 1 to SC 20-06, in which it was determined that the population of control rod blades affected by the underprediction of B-10 in the tip segment included all control rod blades that did not contain Hafnium (Hf) in the tips, not just OEM D-100 control rod blades. This greatly increased the population of control rod blades affected by this issue.

Control rod blades deplete the B-10 isotope as they absorb neutrons when they are inserted into an operating reactor core. Control rod blades are typically fully withdrawn from the core when the reactor is at full power. However, the tips of the control rod blades still experience some thermal neutron flux. The B-10 depletion in the top node of the control rod blade is accounted for in engineering analysis by adding a "tip adder" factor in the B-10 depletion calculation for each control rod blade. Safety Communication SC 20-06 stated that the tip adder factor was much larger than previously calculated, for control rod blades without Hf in the tips. General Electric manufactured control rod blades with Hf tips for a period of time in the 1980s and 1990s that are excluded from the tip adder issue described in SC 20-06. All other control rod blade models, including the OEM blades, are affected by the tip adder issue described in SC 20-06. The higher depletion values in the control rod blade tips for multiple control rod blade types may cause the control rod blade to exceed its effective neutron absorbing capability before the end of the operating fuel cycle. This has the potential to decrease the overall shutdown margin (SDM), which is the ability of all the control rods, except for the most reactive control rod, to shut down the reactor core in all anticipated normal and accident scenarios.

In Revision 1 to SC 20-06, GEH recommended all customers ensure that adequate SDM was available in the current operating fuel cycle until the end of the fuel cycle, once the amount of B-10 depletion was determined in all control rod blade tips. GEH recommended this be done for all General Electric control rod blades that did not contain Hf tips, as well as alternate vendor control rod blades. GEH also recommended all customers assess the impact of control rod blades exceeding their nuclear end of life (NEOL) criteria - the ability of the control rod blade to effectively absorb neutrons - for future fuel cycles beyond the current operating fuel cycle.

Following issuance of GEH SC 20-06, Revision 1, Nine Mile Point Unit 1 entered a refueling outage in March 2021. A control rod blade depletion engineering evaluation was performed, taking into account the new tip adder calculation in SC 20-06. It was determined that two control rod blades that had been located in higher power locations in the previous fuel cycle would be shuffled to two lower power locations in the core for the current Unit 1 operating fuel cycle. No control rod blades in the previous or current fuel cycle have exceeded their NEOL criteria, thus requiring replacement.

In July 2021, Exelon Nuclear Fuels validated that adequate SDM existed for the remainder of the current fuel cycle for Nine Mile Point Unit 2, and that thermal limit margins were not impacted. One control rod blade on the core periphery was predicted to exceed its NEOL criteria due to the tip adder issue described in SC 20-06, before the end of the Unit 2 fuel cycle in March 2022. This blade, along with six other control rod blades, are scheduled for replacement in the upcoming refueling outage. In September 2021, General Electric Global Nuclear Fuels completed an analysis to confirm that SDM would be maintained above the technical specification limit for the remainder of the Unit 2 fuel cycle. Exelon procedure NF-AB-135-1410, "BWR Control Blade Lifetime Management," contains guidance for calculating B-10 depletion in all models of control rod blades currently in operation in the nuclear fleet.

This procedure will require an update to incorporate the new guidance from SC 20-06, for estimating the tip adder factor for non-Hf tipped control rod blades. Issue Report 04242262 is tracking completion of this procedural update.

The inspectors interviewed engineering staff from Exelon Nuclear Fuels and Nine Mile Point Reactor Engineering to discuss corrective actions taken in response to GEH SC 20-06, and reviewed shutdown margin and control rod blade depletion engineering evaluations. The inspectors also reviewed the corrective actions taken and planned for responding to GEH SC 20-06 entered into the corrective action system. No performance deficiencies were identified.

Corrective Action References: 04242262, 04386300,

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On April 21, 2022, the inspectors presented the integrated inspection results to Mr. Peter Orphanos, Site Vice President, and other members of the licensee staff.
  • On February 8, 2022, the inspectors presented the control rod blade technical evaluation problem identification and resolution inspection results to Philip Nichols, Manager Reactor Engineering, and other members of the licensee staff.
  • On March 17, 2022, the inspectors presented the Unit 2 inservice inspection results to Mr. Peter Orphanos, Site Vice President, and other members of the licensee staff.
  • On March 17, 2022, the inspectors presented the radiological hazard assessment and exposure controls inspection results to Mr. Peter Orphanos, Site Vice President, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.01

Procedures

N1-OP-64

Meteorological Monitoring

2100

N2-OP-102

Meteorological Monitoring

2800

OP-AA-108-111-

1001

Severe Weather and Natural Disaster Guidelines

71111.04

Drawings

C-18022-C

Piping & Instrumentation Diagram, Reactor Building Closed

Loop Cooling System

PID-031A, B, E

Piping & Instrumentation Diagram Residual Heat Removal

System

PID-31G

Piping & Instrumentation Diagram Residual Heat Removal

PID-35A

Piping & Instrumentation Diagram Reactor Core Isolation

Cooling

PID-35B

Piping & Instrumentation Diagram Reactor Core Isolation

Cooling

PID-38B

Piping & Instrumentation Diagram Fuel Pool Cooling &

Cleanup

PID-38C

Piping & Instrumentation Diagram Fuel Pool Cooling &

Cleanup

Procedures

N1-OP-11

Reactor Building Closed Loop Cooling System

03400

N2-OP-100A

Standby Diesel Generators

200

N2-OP-100A-

LINEUPS

Standby Diesel Generators - LINEUPS

00500

N2-OP-31

Residual Heat Removal System

03700

N2-OP-31-

LINEUPS

Residual Heat Removal System

003

N2-OP-38

Spent Fuel Cooling and Cleanup System

2700

71111.05

Corrective Action

Documents

04477281

Drawings

B-40143-C

Fire Zones Reactor Building - Fl. El. 261' Turbine Building -

Fl. El. 261' Fire Rated Walls and Slabs

Fire Plans

N2-FPI-PFP-0201

Unit 2 Pre-Fire Plans

71111.06

Corrective Action

Documents

04416206

04477927

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

04661043

71111.07A Corrective Action

Documents

04484882

04486864

Procedures

ER-AA-340-1002

Service Water Heat Exchanger Inspection Guide

S-TDP-REL-0102

Service Water Heat Exchanger and Component Inspection

Guide

Work Orders

C93738267

71111.08G Corrective Action

Documents

04327298

Corrective Action

Documents

Resulting from

Inspection

04484400

Engineering

Evaluations

ECP-20-000224

Recirculation Inlet Nozzle DMW No. 2RPV-KB11 (N2J) Flaw

Evaluation

03/25/2020

Miscellaneous

ER-NM-330-2001

ISI Program Plan Fourth Ten-Year Inspection Interval

Revision 3

ER-NM-330-2004

Risk Informed Inservice Inspection Program Fourth Ten-

Year Inspection Interval

Revision 0

Procedures

ER-AA-335-018

Visual Examination of ASME IWE Class MC and Metallic

Liners of Class CC Components

Revision 15

ER-AA-335-030

Ultrasonic Examination of Ferritic Piping Welds

Revision 5

ER-AA-335-1000

Nondestructive Examination (NDE)

Revision 16

GEH-UT-254

Automated Phased Array Ultrasonic Examination of

Dissimilar Metal Welds with the TOPAZ

Version 1

WPS 8-8-GTSM

Welding Procedure Specification Record for Manual GTAW

and SMAW of P-Number 8 to P-Number 8 Base Metal

Revision 7

71111.11Q Procedures

N1-ST-W1

Control Rod Exercising Operability Test

2300

N2-OP-101C

Plant Shutdown

04100

N2-OP-29

Reactor Recirculation System

03400

N2-OP-31

Residual Heat Removal System

03700

71111.12

Procedures

N2-MSP-EGS-

R001

Diesel Generator Inspection Division 1 and 2

25

Work Orders

C938144677

71111.13

Corrective Action

04481795

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Documents

Procedures

N2-OP-19-

Lineups

Instrument and Service Air Systems

N2-OP-70

Station Electrical Feed and 115KV Switchyard

2800

N2-PM-082

RPV [reactor pressure vessel] Flood-Up/Draindown

01900

OP-NM-108-117

Protected Equipment Program at Nine Mile Point

OP-NM-108-117

Protected Equipment Program at Nine Mile Point

00500

OU-NM-103-101

Shutdown Safety Management Program

0700

71111.15

Calculations

2N3714

Nine Mile Point Nuclear Station Unit 1 TRACG-LOCA

Analysis for GNF2 Fuel

Corrective Action

Documents

04061889

04470659

04475343

04476776

04481649

04482642

04483059

04488015

Drawings

0001040209048

Control Diagram Shutdown System

13.00

Engineering

Changes

ECP-22-000147

Technical Evaluation for MSIV Failed Stroke Time Extent of

Condition

0000

Miscellaneous

NEI 06-09-A

Risk-Informed Technical Specifications Initiative 4b: Risk-

Managed Technical Specifications (RMTS) Guidelines

Purchase Order

00802656

Service, Repair, Refurbishment of MSIV Actuator Air Pack

RICT Record for

March 28, 2022

Failed MSIV 7D RPS Testing

04/06/2022

Procedures

N1-OP-1

Nuclear Steam Supply System

07700

N2-OP-100A

Standby Diesel Generators

03100

N2-OSP-EGS-

M@001

Diesel Generator and Diesel Air Start Valve Operability Test-

Division I and II

24T1

OP-AA-108-118

Risk Informed Completion Time

71111.18

Corrective Action

2547530

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Documents

2689624

04359704

04365824

04428910

04482114

Engineering

Changes

ECP-21-000088

PCIV Supply Nitrogen Line Primary Containment Inboard

Isolation Re-Design

0000

ECP-21-000437

EDG Governor Booster

0000

ECP-21-000454

Digital Electro-Hydraulic Control (DEHC) Low Pass Filter

Modification

Miscellaneous

FAT/SAT Testing for DEHC Low Pass Filter Mod

0000

Procedures

N2-OSP-EGS-

M@0001

Diesel Generator and Diesel Air Start Valve Operability Test

- Division I and II

24T1

Work Orders

C93782709

C93809087

C93813137

71111.19

Corrective Action

Documents

04480094

04481795

04484882

04486059

Corrective Action

Documents

Resulting from

Inspection

04486063

Procedures

GAP-HSC-09

System Aging Inspection and Cleanliness Controls

2000

N2-MSP-EGS-

R001

Diesel Generator Inspection Division I and II

2400

N2-OSP-EGS-

M@0001

Diesel Generator and Diesel Air Start Valve Operability Test

- Division I and II

2400.01

N2-OSP-RHS-

Q@005

RHR System Loop B Pump and Valve Operability Test,

System Integrity Test and ASME XI Pressure Test

01500

N2-OSP-RHS-

R001

Division II ECCS Functional Test

00900

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

S-EPM-GEN-004

Insulation of Power, Control, and Instrument Cable

Connections

00700

Work Orders

C93738267

C93782709

C93814677

C93825512

71111.20

Corrective Action

Documents

04482986

04482995

04483785

04484026

04484553

04485270

Corrective Action

Documents

Resulting from

Inspection

04484400

04486063

Miscellaneous

NM2C19-SU

Reactivity Maneuver Plan

Procedures

LS-AA-119

Fatigue Management and Work Hour Limits

N2-FHP-13.3

Core Shuffle

200

N2-OP-101A

Plant Start-up

05400

N2-OP-38

Spent Fuel Cooling and Cleanup System

2700

N2-OSP-NMS-

@002

Source Range Monitor Check During Core Offload/Reload

201

OP-AA-109-101

Personnel and Equipment Tagout Process

OP-AA-300

Reactivity Management

OP-AA-300-1520

Reactivity Management - Fuel Handling, Storage and

Refueling

OU-NM-103-101

Shutdown Safety Management Program

00700

OU-NM-4001

Refueling Operations

00800

71111.22

Corrective Action

Documents

04481649

04482027

04483059

04483200

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

04483399

04485322

Miscellaneous

Technical

Evaluation N2R18

MSIV Leak Rate Tests

Approved

03/17/2022

Procedures

N1-ST-M4A

Emergency Diesel Generator 102 and PB 102 Operability

Test

03000

N1-ST-Q1A

CS 111 Pump, Valve and SDC Water Seal Check Valve

Operability Test

200

N2-ISP-RRC-

R001

ARI [alternate rod insertion] function of RRCS [redundant

reactivity control system]

00700

N2-OSP-ADS-

R002

ADS System Functional Test and Remote Shutdown System

Test

009

N2-OSP-CSL-

Q@002

LPCS Pump and Valve Operability and System Integrity

Test

01500

N2-OSP-EGS-

R001

Diesel Generator ECCS Start and Load Reject Division II

N2-OSP-ICS-

Q@002

RCIC Pump and Valve Operability Test and System Integrity

Test and ASME XI Functional Test and Analysis

01600

N2-OSP-MSS-

003

Main Steam Isolation Valve Leak Rate Test

00300

N2-OSP-MSS-

004

Main Steam Isolation Valve Leak Rate Test (Reactor Vessel

Head Removed)

200

N2-OSP-MSS-

CS001

Main Steam Isolation Valve Operability Test

01000 and

01100

N2-OSP-SLS-

R001

Standby Liquid Control Manual Initiate Actuation and ASME

XI Pressure Test

01100

71151

Procedures

NEI 99-02

Regulatory Assessment Performance Indicator Guideline

71152A

Corrective Action

Documents

242262

04386300

04436618

Engineering

Evaluations

ECP-20-000291

Control Blade Replacement Strategy for Nine Mile Point Unit

Cycle 25 (Reload 26)

ECP-21-000248

Control Blade Replacement Strategy for Nine Mile Point Unit

(Reload 18)

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

ECP-21-000380

SC 20-06: Nine Mile Point Unit 2 Cycle 18 SDM and

MSBWP Evaluation

Miscellaneous

General Electric

Hitachi Safety

Communication

20-06, Rev. 1

Impact of Ex-core Flux on Control Rod Lifetime Limits

2/26/2021

Procedures

NF-AB-130-3690

Maximum Subcritical Banked Withdrawal Position

NF-AB-135-1410

BWR Control Blade Lifetime Management

16