PNO-IV-88-070, on 880825,reactor Scrammed Due Trip of Main Turbine After Brush Failure of Main Generator Exciter. Although Water Level Has Not Dropped to Level 2,HPCS Pump Did Start & May Have Injected.Power Restored to Div III Bus

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PNO-IV-88-070:on 880825,reactor Scrammed Due Trip of Main Turbine After Brush Failure of Main Generator Exciter. Although Water Level Has Not Dropped to Level 2,HPCS Pump Did Start & May Have Injected.Power Restored to Div III Bus
ML20153B862
Person / Time
Site: River Bend Entergy icon.png
Issue date: 08/25/1988
From: Madsen G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
References
PNO-IV-88-070, PNO-IV-88-70, NUDOCS 8808310126
Download: ML20153B862 (1)


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August 25, 1988 PRELIMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE -- PNO-IV-60 /0 This preliminary notification constitutes EARLY notice of events of POSSIBLE safety or public interest significance. The information is as initially received-without verification or evaluation, and is basically all that is known by the Region IV staff on this date.

FACILITY: Gulf States Utilities Licensee Emergency Classification:

River Bend Station X' Notification of Unusual Event DN: 50-458 Alert Site Area Emergency General Emergency Not Applicable

SUBJECT:

OUTAGE GREATER THAN 2 DAYS On August 25, 1988, at 12:32 p.m. (CDT), the reactor scrammed from 100 percent power. The main generator exciter experienced a brush failure which resulted in a trip of the main turbine. The turbine trip initiated the reactor scram. A fast transfer from the normal to the preferred transformer did not occur on the Division III bus. The Division III (high pressure core spray) emergency diesel generator started and closed onto the bus as expected. Although the reactor vessel water level does not appear to have dropped to the Level 2 (HPCS initiation setpoint), the HPCS pump did start and may have injected briefly.

The licensee declared a NOUE because of the HPCS system injection. The licensee secured from the NOVE event at approximately 1:25 p.m. (CDT). Preferred power has been restored to the Division III bus. Reactor pressure is being controlled by the bypass valves and level maintained utilizing one reactor fuel pump and the startup regulating valve. Reactor shutdown is expected to exceed 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.

The NRC has not issued a press release. ,

Neither the licensee nor the NRC plans to issue a press release.

The state of Louisiana has been informed.

Region IV received notification of this occurrence by telephone from the headquarters duty officer.

This information has been confirmed with a licensee representative.

CONTACT: G. L. Madsen, FTS 728-8134 DISTRIBUTION: 1 H. St. MNBB OWF MAIL: DCS(OriginalIE34) l Chairman Zech XEOU EDU DUT-(Transonly} l Conn. Roberts 0IA OGC 1 Comm. Carr NL PA FAX: INP0 l l

Comm. Rogers RES 01 USAC GECY NMSS RRI CA NRR NRC OC PDR SLITP LICENSEE (ReactorLic.) 1 OGC-H A 5520:/JI880

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