PNO-II-86-031, on 860425,w/unit at 85% Power,Reducer Section of Extraction Steam Line Running to Feedwater Heater Ruptured,Leaving Opening in Pipe Over 18 Inches Long.Caused by Moisture in Excitation Sys

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PNO-II-86-031:on 860425,w/unit at 85% Power,Reducer Section of Extraction Steam Line Running to Feedwater Heater Ruptured,Leaving Opening in Pipe Over 18 Inches Long.Caused by Moisture in Excitation Sys
ML20210N907
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 04/25/1986
From: Ignatonis A, Sinkule M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
References
PNO-II-86-031, PNO-II-86-31, NUDOCS 8605050320
Download: ML20210N907 (2)


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  • April 25, 1986 PRELIMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE PN0-II-86-31 This preliminary notification constitutes EARLY notice of events of POSSIBLE safety or public interest significance. The information is as initially received without verifi-cation or evaluation, and is basically all that is known by the Region II staff on this date.

FACILITY: Georgia Power Company Licensee Emergency Classification:

Hatch Unit 2 Notification of Unusual Event Docket No. 50-366 Alert Baxley, Georgia Site Area Emergency General Emergency X Not Applicable

SUBJECT:

UNSCHEDULED SHUTDOWN GREATER THAN 48 HOURS A reducer section of an extraction steam line running to a feedwater heater ruptured about 12:10 a.m.-(EST) today while Hatch Unit 2 was at 85 percent power, leaving an opening in the 4 pipe about 18 inches long and a quarter-inch wide. Moisture from this low-pressure steam leak is believed to have entered the main generator excitation system, causing a turbine trip and a reactor trip about 12:32 a.m. All systems functioned normally during the j shutdown. The steam leak was halted by the closing of the turbine stop and control valves.

No personnel injuries or contamination occurred. Although radiation levels increased above normal operating levels in the turbine building, the releases remained within technical l

sp:cification limits. There was no off-site release in excess of limits.

Georgia Power is continuing to assess both the cause of the event and the extent of the damage. The unit is expected to be out of service for several days. The rupture of this 20-inch-dianeter, non-safety-related steam line is believed to have resulted from erosion /

corrosion of the carbon steel pipe's thin wall. Equivalent piping will be inspected in

{ Hatch Unit 1, which is shut down for refueling, before that unit restarts.

4 GIorgia Power has issued a news release in the innediate plant area, i

j' The State of Georgia has been informed.

G:orgia Power informed the NRC headquarters duty officer of this incident at 2:28 a.m.

today.

! This information is current as of 3 p.m.

Contact:

A. Ignatonis, 242-5563 M. Sinkule, 242-5506 l

g50 20 860425 PNO-II-86-031 PDR '

O ZE3Y

DIITRIBUTION:

H. Street MNBB Phillips E/W Willste MAIL:

Chairman Palladino N NRR T NMSS AURiiDMB Com. Roberts PA OIA RES DOT: Trans Only Com. Asselstine MPA AE0D Applicable State Com. Bernthal ELD Com. Zech Air Rights INP0 - /4,'/2 SECY SP NSAC ACRS R Regions: $7-/u23,sf0-/b:2 V 5 ~# '

Licensee: /O.*f/

(Reactor Licensees)

Applicable Resident Site eteI*'## M## g., A j f stan' vo .s.Ve .