ML20237C277

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Submits Special Rept Re Steam Generator Tube Plugging. End-of-cycle 1 Eddy Current Insp Completed on 871124.Total of 2,054 Tubes Insp.No Flaws Greater than or Equal to Tech Spec Limit of 40% Throughwall Identified.Summary Table Encl
ML20237C277
Person / Time
Site: Millstone Dominion icon.png
Issue date: 12/14/1987
From: Scace S
NORTHEAST NUCLEAR ENERGY CO., NORTHEAST UTILITIES
To:
NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM)
References
MP-11230, NUDOCS 8712210219
Download: ML20237C277 (2)


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NORTHEAST UTILETIES cenerei Omce . semen street. Beron. Connecticut  !

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, (203) 665-5000 December 14, 1987 MP-11230 U.S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555

Reference:

Facility Operating License No NPF-44, Docket No. 50-423 Gentlemen: I STEAM GENERATOR TUBE PLUGGING This special report is being submitted within 15 days pursuant to Millstone Unit 3 Technical Specification Section 4.4.5.5.a. Plant Technical Specifica-tion 4.4.5.5.a requires a special report be submitted to the NRC following the completion of each inservice inspection of steam generator tubes and the number of tubes plugged in each steau generator.

The end-of-cycle I eddy current inspection was completed on November 24, 1987.

Table 1 summarizes the results. A total of 2,054 tubes (9 percent of total) were inspected from all four steam generators. No flaws greater than or equal to the Technical Specification plugging limit of 40 percent throughwall (TW) were identified; however, 2 tubes were plugged on a discretionary basis (Steam Generator A Row 50 Column 94, and Steam Generator D Row 48 Column 98). These tubes exhibited flaws of 34 percent and 32 percent TW, respectively and were located adjacent to antivibration bars.

The complete results of the steam generator tube inservice inspection will be submitted within 12 months in accordance with Plant Technical Specification 4.4.5.5.b.

The licensee contact for this special. report is Larry Loomis who may be reached at (203) 444-5468.

Very truly yours, NORTHEAST NUCLEAR ENERGY COMPANY

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Ste hen 3 Scace Station Superintendent Millstone Nuclear Power Station SES/LEL:cjh Attachment cc: W. T. Russell, Region 1 W. J. Raymond, Senior Resident Inspector h d

8712210219 871214

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.c TABLE 1

-MILLSTONE 3 1987 EDDY CURRENT INSPECTION

SUMMARY

Total SGA SGB SCC SGD Total Tubes- 22,504 5.626 5,626 5,626 5,626 Tubes Inspected 2,054 .543 501 506 504  !

Tubes With Maximum Flaw

>40 Percent.(Defect) 0 0 0 0 0 Tubes With Maximum Flaw-

<40 Percent but >20 Percent 24 12 2 3 ,

Tubes Plugged As A '

Result Of This Inspection 2 1 0 0 ,1 3

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