ML20127K823

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Special Rept:On 921015,motor-driven Fire Pump 1FP-P-1 Tagged Out & Removed from Svc for More than 7 Days to Permit Maint Activities.Fire Pump Returned to Svc on 921031 & Cross Tie to Fire Loop Will Be Opened When Fire Pump Out of Svc
ML20127K823
Person / Time
Site: North Anna  Dominion icon.png
Issue date: 11/18/1992
From: Stewart W
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
92-703, NUDOCS 9211230257
Download: ML20127K823 (2)


Text

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. VIRGIN 1 A El.ECTRIC AND POWER CObf PANY RICMtOND. VlHOINIA 23001 Novemter 18, 1992 U.S. Nuclear Regulatory Commiss!on Serial No.92-703 Attention: Document Control Desk MPW/EJW Washington, D.C. 20555 Docket Nos. 50-338 50-309 License Nos. NPF-4 NPF-7 Gentlemen:

VIRGINIA ELECTRIC AND POWER COMPANY NORTH ANNA POWER STATION UNITS 1 & 2 FIRE PUMP 087 OF SERVICF, GRE ATER TH AN 7 DAYS SPECIAL REPORT Pursuant to Updated Final Safety Analysis Report (UFSAR) Technical Requirement 1r.2.1.2.1.A.2, a Special Report is required because the motor driven fire pump has been out of service for greater than 7 days. On October 15,1992, at 0815 hours0.00943 days <br />0.226 hours <br />0.00135 weeks <br />3.101075e-4 months <br />, the motor driven fire pump,1-FP-P-1, was tagged out and removed from service as a safety precaution to facilitate maintenance activities on the "A" Circulating Water (CW) pump,1-CW-P-1 A.

The recirculating discharge of the fire pump empties into the "A" CW bay where maintenance activities are being performed. The fire pump was removed from service, because personnel working in the "A" CW bay cou'd be subjected to flooding conditions should the fire pump enter a recirculation condition. The fire pump remained out of service until the CW pump removal was completed. Fire pump 1-FP-

!) P-1 was returned to service at 0418 hours0.00484 days <br />0.116 hours <br />6.911376e-4 weeks <br />1.59049e-4 months <br /> on October 31,1992.

To provide for a loss of redundancy, with 1-FP-P-1 out of service, a motor driven fire pump,1-FW-P-11, is main:ained operable and the cross tie to the plant fire loop is

, opened. The cross lie to the plant fire loop will be opened when i-FP-P-1 is out of service.

Once the CW pump inspection and rebuilding are completed and ready for reinstallation, the fire pump w:ll again be taken out of service. The reinstallation activities of the CW pump are expected to last greater than 7 days. As such the UFSAR Technical Requirement 16.2.1.2.1.A.2 will be exceeded again during reinstallation of the "A" CW pump. Therefore, notification of the scheduled fire pump inoperability is being included as a part of this Special Report.

9211230257 921118 /

e PDR S

ADOCK 05000339 PDR A

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1. h' f RIP f U i s

This Special Report has been reviewed by the Station Nuclear Safety and Operating Committee and will be provided to the Management Safety Review Committee.

Should you have any questions regarding this report, please contact us.

Very truly yours, s ,

\,JL , y W. L. Stewart Senior Vice President - Nuclear cc: U.S. Nuclear Regulatory Commission Region 11 101 Marietta Street, N.W.

Suite 2900 Atlanta, Georgia 30323 Mr. M. S. Lesser

=

NRC Senior Resident inspector North Anna Power Station

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