ML20080H981

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RO SP-N1-84-01:on 840109,I-131 Dose Equivalent Specific Activity Exceeded Tech Spec Limit.Caused by Minor Fuel Element Defects in Reactor Core.Primary Coolant Sampled & Analyzed at Accelerated Frequency
ML20080H981
Person / Time
Site: North Anna Dominion icon.png
Issue date: 02/01/1984
From: Harrell E
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
References
N-84-01, N-84-1, RO-SP-N1-84-01, RO-SP-N1-84-1, NUDOCS 8402140406
Download: ML20080H981 (16)


Text

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4 VIRGINI A ELECTRIC AND POWER COMPANY NORTH ANN A POWER ST ATION P. o. BOX 402 MINERAL, VIRGINI A 23117 February 1,1984 Mr. James P. O'Reilly, Regional Administrator Serial No. N-84-01 U. S. Nuclear Regulatory Commission N0/JRR: 11 Region II Dochet No. 50-338 101 Marietta Street, Suite 2900 Atlanta, Georgia 30303 License No. NPF-4

Dear Mr. O'Reilly:

Pursuant to North Anna Power Station Technical Specifications, the Virginia Electric and Power Company hereby submits the following Special Raport applicable to North Anna Unit No. 1.

Report No. Applicable Technical Specificatinns Special Report SP-N1-84-01 T.S. 6.9.2.f This report has been reviewed by the Station Nuclear Safety and Operating Committee and will be forwarded to Safety Evaluation and Control for their review.

Very Truly Yours, E. Wayne . e Station anager Enclosures (3 copies) cc: Document Control Desk (1 copy) 016 Phillips Bldg.

U.S. Nuclear Regulatory Commission Washington, D. C. 20555 OFFICIAL COPY

/t v 7 R $m 8402140406 840201 d'I " ' ['

DESicHATED OHIGINAL s RADocnosoooQ Certitled By FAIEd

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T Virginia Electric and Power Company North Anna Power Station, Ur.it No. 1 Page 1 of 2 Docket No. 50-338 Special Report No. SP-N1-84-01 Description of Event On January 9, 1984 at 0603 fellowing a unit rampdown, the I-131 Dose Equivalent specific activity exceeded 1.0 microcurie / gram. The specific activity returned to wichin the T.S. 3.4.8 limit by 0345 on January 10, 1984. This event is reportable as a Special Report pursuant to T.S. 6.9.2.f.

Probable Consequences of Occurrence Primary coolant I-131 Dose Equivalent specific activity peaked at 1.64 microcurie / gram at 1110 on January 9, 1984, and returned to within limits by 0345 on January 10, 1984. Daily samples taken prior to the rampdown were consistently less than 0.1 microcurie / gram Dose Equivalent

- I 131. The primary coolant Dose Equivalent I-131 exceeded the !.0 microcurie / gram limit for a time period less than or equal to 22 hours2.546296e-4 days <br />0.00611 hours <br />3.637566e-5 weeks <br />8.371e-6 months <br />.

The 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> sampling surveillance frequency required by T.S. Table 4.4-4 was maintained throughout the event. The health and safety of the public were not-affected.

Cause of Event On January 8, 1984 at approximately 2318, a unit rampdown was initiated as a result of a suspected unidentified Reactor Coolant System

- leakage greater than 1 gallon / minute. - At 0516 on January 9, 1984 the turbine was manually tripped while the reactor was maintained critical at 1 percent power. The reactor was maintained at this power level until 2200 when it was shutdown by manually insertina control rods.

The increase in Dose Equivalent I-131 activity occurred as a result of known, but nc,t specifically ' identified, minor fuel element defects present in the reactor core. The diffusion of iodine into the reactor coolant was enhanced by the rapid decrease in reactor power. Iodine spiking with power. changes is a well documented and accepted phenomenon.

Immediate Corrective Action The primary coolant was sampled and analyzed at the accelerated frequency required by Item 4a of Technical Specification 3.4.8, Table 4.4-4.

Scheduled Corrective Action None are required.

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. s Special Report SP-N1-84-01 Page 2 of 2 Action Taken To Prevent Recurrence Iodine spiking from minor fuel defects following rapid power changes is expected. Unit I reactor powa.r change rates durf ng normal operation have been administrative 1y limited to reduce the ptobability of recurrence.

Generic Implications Iodine spiking as a recurring phenomenon in Unit 1 and has been previously reported.

Attachment:

Page 1 of 3 Supplemental Information This event is reportable as a "Special Report" pursuant to T.S.

6.9.2. In addition the supplemental inforestion required by T.S. 3.4.8 is included as foilews:

1. Reactor Power History 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> prior to the event:

DATE TIME POWER MWe COEIENTS 01-06-84 0000-2400 100% 940 a 01-07-84 0000-2200 100% 940 a 01-08-84 0000 93% 877 b 01-08-84 0100 91.5% 866 b 01-08-84 0300 98.2% 921 b 01-08-84 0500-2300 100% 940 a 01-09-84 0000 92% 869 c 01-09-84 0300 42.1% 376 c 01-09-84 0511 5.4% 24 c 01-09-84 0521 1.0% 0 d 01-09-84 1200 1.0% 0 e 01-09-84 2151 1.0% 0 f 01-09-84 2200 0% 0 g a) Steady state power operation.

b) Reactor / Turbine power decrease in order to perform Turbine Valve Freedom Test.

c) Began rampdown at 2318 due to suspected Unidentified Reactor Coolant System leakage >1.0 gallon / minute.

d) Turbine manually tripped at 0516 while maintaining reactor critical in Mode 2.

e) Reac::or maintained critical in Mode 2.

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Attachment:

Page 2 of 3 f) Reactor shutdown commenced by manually inserting control rods.

g) Reactor shutdown.

2. Fuel Burnup by Core Region - As of January 8, 1984:

FUEL BATCH BURNUP (MWD /MTU) 4A2 32,092.9 5A 25,186.7 6A 11,027.5

3. One mixed bed demineralizer was in service from 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> prior to the event until 1615 on January 8, 1984. At that time the demineralizer was bypassed in an effort to locate the cause of the unidentified RCS leakage. The demineralizer was raturned to service at 2325 on January 8, 1984 and remained in service during and following the event. The average flowrate through the demineralizer when it was inservice was 127 gpm.
4. No de-gassing operations were performed.
5. Duration of Dose Equivalent I-131 above 1.0 microcurie / gram:

DOSE EOUIVALENT DATE TIME I-131 (MICR0 CURIES / GRAM) 01-07-84 0212 0.0769 01-08-84 0148 0.0985 01-09-84 0158 0.176 01-09-84 0603 1.14 01-09-84 0915 1.53 01-09-84 1110 1.64 01-09-84 1355 1.41

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Virginia Electric and Power Company North Anna Power Station, Unit No. 1 Page 1 of 2 Docket No. 50-338 Special Report No. SP-N1-84-01 Description of Event On January 9, 1984 at 0603 following a unit rampdown, the I-131 Dose Equivalent specific activity exceeded 1.0 microcurie / gram. The specific activity returned to within the T.S. 3.4.8 limit by 0345 on January 10, 1984. This event is reportable as a Special Report pursuant to T.S. 6.9.2.f. ,

Probable Consequencea of Occurrence Primary coolant 1-131 Dose Equivalent specific activity peaked at 1.64 microcurie / gram at 1110 on January 9, 1984, and returned to within limits by 0345 on January 10, 1984. Daily samples taken prior to the rampdown were consistently lees than 0.1 nicrocurie/ gram Dose Equivalent I-131. The primary coolant Dose Equivalent I-131 exceeded the 1.0 microcurie / gram limit for a time period less than or equal to 22 hours2.546296e-4 days <br />0.00611 hours <br />3.637566e-5 weeks <br />8.371e-6 months <br />.

The 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> sampling surveillance frequency required by T.S. Table 4.4-4 was maintained throughout the event. The health and safety of the public were not affected.

Cause of Event On January 8, 1984 at approximately 2318, a unit rampdown was initiated as a result of a suspected unidentified Reactor Coolant System leakage greater than 1 gallon / minute. At 0516 on January 9, 1984 - the turbine was manually tripped while the reactor was maintained critical at 1 percent power. The reactor was maintained at this power level until 2200 when it was shutdown by manually inserting control rods.

The increase in Dose Equivalent I-131 activity occurred as a result of known, but not specifically identified, minor fuel element defects present in the reactor core. The diffusion of iodine into the reactor coolant was enhanced by the rapid decrease in reactor power. Iodine spiking with power changes is a well documented and accepted phenomenon.

Immediate Corrective Action The primary coolant was sampled and analyzed at the accelerated frequency required by Item 4a of Technical Specification 3.4.8, Table 4.4-4.

Scheduled Corrective Action None are required.

Special Report SP-N1-84-01 Page 2 of 2 Action Taken To Prevent Recurrence Iodine spiking from minor fuel defects following rapid power changes is expected. Unit I reactor power change rates during normal operation have been administratively limited to reduce the probability of recurrence. .

Generic Implications Iodine spiking as a recurring phenomenon in Unit 1 and has been previously reported.

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Attachment:

Page 1 of 3 Supplemental Information This event is reportable as a "Special Report" pursuant to T.S.

6.9.2. In addition the supplemental information required by T.S. 3.4.8 is included as follows:

1. Reactor Power History 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> prior to the event:

DATE TIME POWER MWe COMMENTS 01-06-84 0000-2400 100% 940 a 01-07-84 0000-2200 100% 940 a 01-08-84 0000 93% 877 b 01-08-84 0100 91.5% 866 b 01-08-84 0300 98.2% 921 b 01-08-84 0500-2300 100% 940 a 01-09-84 0000 92% 869 c 01-09-84 0300 42.1% 376 c 01-09-84 0511 5.4% 24 c 01-09-84 0521 1.0% 0 d 01-09-84 1200 1.0% 0 e 01-09-84 2151 1.0% 0 f 01-09-84 2200 0% 0 g a) Steady state power operation.

b) Reactor / Turbine power decrease in order to perform Turbine Valve Freedom Test.

c) Began rampdown at 2318 due to suspected Unidentified Reactor Coolant System leakage >1.0 gallon / minute.

d) Turbine manually tripped at 0516 while maintaining reactor critical in Mode 2.

e) Reactor maintained critical in Mode 2.

Attachment:

Page 2 of 3 f) Reactor shutdown commenced by manually inserting control rods.

g) Reactor shutdown.

2. Fuel Burnup by Core Region - As of January 8, 1984:

FUEL BATCH BURNUP (MWD /MTU) 4A2 32,092.9 SA 25,186.7 6A 11,027.5

3. One mixed bed demineralizer was in service from 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> prior to the event until 1615 on January 8, 1984. At that time the demineralizer was bypassed'in an effort to locate the cause of the unidentified RCS leakage. The demineralizer war returned to service at 2325 on January 8, 1984 and remained in service during and following the event. The average flowrate through the demineralizer when it was inservice was 127 gpm.
4. No de-gassing operations were performed.
5. Duration of Dose Equivalent I-131 above 1.0 microcurie / gram:

DOSE EQUIVALENT DATE TIME I-131 (MICR0 CURIES / GRAM) 01-07-84 0212 0.0769 01-08-84 0148 0.0985 01-09-84 0158 0.176 01-09-84 0603 1.14 01-09-84 0915 1.53 01-09-84 1110 1.64 01-09-84 1355 1.41 l.

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Virginia Electric and Power Company North Anna Power Station, Unit No. 1 Page 1 of 2 Docket No. 50-338 Special Report No. SP-N1-84-01 Description of Event On January 9, 1984 at 0603 following a unit rampdown, the I-131 Dose Equivalent specific activity exceeded 1.0 microcurie / gram. The specific activity returned to within the T.S. 3.4.8 limit by 0345 on L y 10, 1984. This event is reportable as a Special Report pursuant to T.S. 6.9.2.f.

Probable Consequences of Occurrence Primary coolant I-131 Dose Equivalent specific activity peaked at 1.64 microcurie / gram at 1110 on January 9, 1984, and returned to within limits by 0345 on January 10, 1984. Daily samples taken prior to the rampdown were consistently less than 0.1 microcurie / gram Dose Equivalent I-131. The primary coolant Dose Equivalent I-131 exceeded the 1.0 microcurie / gram limit for a time period less than or equal to 22 hours2.546296e-4 days <br />0.00611 hours <br />3.637566e-5 weeks <br />8.371e-6 months <br />.

The 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> sampling sutveillance frequency required by T.S. Table 4.4-4 was maintained throughout the event. The health and safety of the public were not affected.

Cause of Event On January 8, 1984 at approximately 2318, a unit rampdown was initiated as a result of a suspected unidentified Reactor Coolant System leakage greater than 1 gallon / minute. At 0516 on January 9, 1984 the turbine was manually tripped while the reactor was maintained critical at 1 percent power. The reactor was maintained at this power level until 2200 when it was shutdown by manually inserting control rods.

The increase in Doae Equivalent I-131 activity occurred as a result of known, but not specifically identified, minor fuel element defects present in the reactor core. The diffusion of iodine into the reactor coolant was enhanced by the rapid decrease in reactor power. Iodine spiking with power changes is a well documented and accepted phenomenon.

Immediate Corrective Action The primary coolant was sampled and analyzed at the accelerated frequency required by Item 4a of Technical Specification 3.4.8, Table 4.4-4.

Scheduled Corrective Action l

None are required.

Special Report SP-N1-84-01 Page 2 of 2 Actien Taken To Prevent Recurrence Iodine spiking from minor fuel defects following rapid power changes is expected. Unit I reactor power change rates during normal operation have been administrative 1y limited to reduce the probability of recurrence.

Generic Implications

-Iodine spiking as a recurring phenomenon in Unit 1 and has been previously reported.

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Attachment:

Page 1 of 3 Supplemental Information This event is reportable as a "Special Report" pursuant to T.S.

6.9.2. In addition the supplemental information required by T.S. 3.4.8 is included as follows:

1. Reactor Power History 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> prior to the event:

DATE TIME POWER MWe COMMENTS 01-06-84 0000-2400 100% 940 a 01-07-84 0000-2200 100% 940 a 01-08-84 0000 93% 877 b 01-08-84 0100 91.5% 866 b 01-08-84 0300 98.2% 921 b 01-08-84 0500-2300 100% 940 a 01-09-84 0000 92% 869 c 01-09-84 0300 42.1% 376 e 01-09-84 0511 5.4% 24 c 01-09-84 0521 1.0% 0 d 01-09-84 1200 1.0% 0 e 01-09-84 2151 1.0% 0 f 01-09-84 2200 0% 0 g e) Steady state power operation.

b) Reactor / Turbine power decrease in order to perform Turbine Valve Freedom Test.

c) Began rampdown at 2318 due to suspected Unidentified Reactor Coolant System leakage >1.0 gallon / minute.

d) Turbine manually tripped at 0516 while maintaining reactor critical in Mode 2.

e) Reactor maintained critical in Mode 2.

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Attachment:

Page 2 of 3 f) Reactor shutdown commenced by manually inserting control rods, g) Reactor shutdown.

2. Fuel Burnup by Core Region - As of January 8, 1984:

FUEL BATCH BURNUP (MWD /MTU) 4A2 32,092.9 SA 25,186.7 6A 11,027.5

3. One mixed bed demineralizer was in service from 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> prior to the event until 1615 on January 8, 1984. At that time the demineralizer was bypassed in an effort to lorate the cause of the unidentified RCS leakage. The demineralizer was returned to service at 2325 on January 8, 1984 and remained in service during and following the event. The average flowrate through the demineralizer when it <as inservice was 127 gpm.
4. No de-gassing operations were performed.
5. Duration of Dose Equivalent I-131 above 1.0 microcurie / gram:

DOSE EOUIVALENT DATE TIME I-131 (MICR0 CURIES / GRAM) 01-07-84 0212 0.0769 01-08-84 0148 0.0985 01-09-84 0158 0.176 01-09-84 0603 1.14 01-09-84 0915 1.53 l 01-09-84 1110 1.64 01-09-84 1355 1.41

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