|
---|
Category:CORRESPONDENCE-LETTERS
MONTHYEARSVP-99-181, Forwards Biennial Update to Quad Cities Ufsar,Iaw 10CFR50.71(e).Update Includes Changes to Facility & Procedures & Are Current Through 9906301999-10-20020 October 1999 Forwards Biennial Update to Quad Cities Ufsar,Iaw 10CFR50.71(e).Update Includes Changes to Facility & Procedures & Are Current Through 990630 ML20217H4661999-10-18018 October 1999 Forwards Changes to EPIPs IAW 10CFR50.54(q) & 10CFR50,App E, Section V.Details of Changes Encl ML20217K7011999-10-13013 October 1999 Provides Response to Questions Related to Request for License Amend,Per 10CFR50.90, Credit for Containment Overpressure. Supporting Calculations Encl 05000254/LER-1999-004, Forwards LER 99-004-00,IAW Requirements of 10CFR50.73(a)(2)(i)(B).Util Is Committed to Listed Action1999-10-12012 October 1999 Forwards LER 99-004-00,IAW Requirements of 10CFR50.73(a)(2)(i)(B).Util Is Committed to Listed Action ML20217F6321999-10-0707 October 1999 Forwards Insp Repts 50-254/99-01 & 50-265/99-01 on 990721- 0908.No Violations 05000254/LER-1999-003, Forwards LER 99-003-00 IAW 10CFR73(a)(2)(v)(A).Commitment Made by Util,Listed.Any Other Actions Described in LER Represent Intended or Planned Actions by Licensee1999-10-0707 October 1999 Forwards LER 99-003-00 IAW 10CFR73(a)(2)(v)(A).Commitment Made by Util,Listed.Any Other Actions Described in LER Represent Intended or Planned Actions by Licensee ML20212K9421999-10-0505 October 1999 Informs That NRC Accepts 990513 Inservice Inspection Relief Request CR-31 for Quad Cities Nuclear Power Station,Units 1 & 2 ML20216J8241999-09-30030 September 1999 Notifies of Removal of NRC Headquarters & Region III Offices from Controlled Copy Distribution of Certain CE Documents. Specific Documents,Associated Controlled Copy Numbers & NRC Location Affected Are Shown on Attachment to Ltr SVP-99-189, Confirms Completion of Actions Identified During Review of NRC Safety Evaluation of Boiling Water Reactor Owners Group Rept, Utility Resolution Guidance of ECCS Suction Strainer Blockage1999-09-22022 September 1999 Confirms Completion of Actions Identified During Review of NRC Safety Evaluation of Boiling Water Reactor Owners Group Rept, Utility Resolution Guidance of ECCS Suction Strainer Blockage ML20212J0451999-09-21021 September 1999 Forwards Safety Evaluation of Licensee USI A-46 Program at Quad Cities Nuclear Power Station,Units 1 & 2,established in Response to GL 87-02 Through 10CFR50.54(f) Ltr ML20212D8231999-09-20020 September 1999 Informs That Effectieve 991101,NRC Region III Will Be Conducting Safety System Design & Performance Capability Pilot Insp at Quad Cities Nuclear Power Station.Insp Will Be Performed IAW NRC Pilot Insp Procedure 71111-21 ML20212C6961999-09-15015 September 1999 Forwards Insp Repts 50-254/99-17 & 50-265/99-17 on 990823- 0827.No Violations Noted SVP-99-190, Clarifies Statement Contained in NRC Insp Repts 50-254/99-12 & 50-265/99-12,dtd 990813,paragraph 4OA1.3B, Observation & Findings, Re Sys Mod to DG Air Start Sys1999-09-13013 September 1999 Clarifies Statement Contained in NRC Insp Repts 50-254/99-12 & 50-265/99-12,dtd 990813,paragraph 4OA1.3B, Observation & Findings, Re Sys Mod to DG Air Start Sys ML20211Q7961999-09-0909 September 1999 Forwards Correction to Administrative Error on Page 8 of NRC Insp Repts 50-254/99-16 & 50-265/99-16,transmitted by Ltr, ML20217H5661999-09-0909 September 1999 Discusses 990907 Pilot Plan Mgt Meeting Re Results to-date of Pilot Implementation of NRC Revised Reactor Oversight Process at Prairie Island & Quad Cities.Agenda & Handouts Provided by Utils Encl ML20211Q6511999-09-0808 September 1999 Informs That NRC Tentatively Scheduled Initial Licensing Exam for Quad Cities Operator License Applicants During Wk of 000327.Validation of Exam Will Occur at Station During Wk of 000306 ML20211G1221999-08-27027 August 1999 Forwards fitness-for-duty Program Performance Data for Each of Comm Ed Nuclear Power Stations & Corporate Support Employees within Scope of Rule for six-month Period Ending 990630,IAW 10CFR26.71(d) ML20211F8251999-08-25025 August 1999 Forwards Insp Repts 50-254/99-15 & 50-265/99-15 on 990816-20.No Violations Noted.Insp Evaluated Effectiveness of Maint Rule Program & Review Periodic Evaluation Specifically Required for 10CFR50.65 ML20211B8691999-08-20020 August 1999 Forwards Insp Repts 50-254/99-10,50-265/99-10,50-454/99-09, 50-455/99-09,50-456/99-10 & 50-457/99-10 on 990628-0721. Action Plans Developed to Address Configuration Control Weaknesses Not Totally Effective as Listed ML20211D1491999-08-19019 August 1999 Forwards Insp Repts 50-254/99-16 & 50-265/99-16 on 990719-22.Staff Identified Major Discrepancy Re Accuracy of Data Submitted to NRC for Protected Area Security Equipment Performance ML20211C7601999-08-19019 August 1999 Confirms NRC Intent to Meet with NSP & Ceco on 990807 in Lisle,Il to Discuss with Region III Pilot Plants,Any Observations,Feedback,Lessons Learned & Recommendations Relative to Implementation of Pilot Program ML20210R7451999-08-13013 August 1999 Forwards Insp Repts 50-254/99-11 & 50-265/99-11 on 990601-0720.NRC Identified Several Issues Which Were Categorized as Being of Low Risk Significance.Two Issues Involved NCVs of Regulatory Requirements SVP-99-147, Notifies of Change to Bases of TS to Licenses DPR-29 & DPR- DPR-30.Change to TS Section 3/4.9 Provides Clarity & Consistency with Sys Design Description in Ufsar,Sections 8.3.2.1 & 8.3.2.2.TS Bases Page,Encl1999-08-13013 August 1999 Notifies of Change to Bases of TS to Licenses DPR-29 & DPR- DPR-30.Change to TS Section 3/4.9 Provides Clarity & Consistency with Sys Design Description in Ufsar,Sections 8.3.2.1 & 8.3.2.2.TS Bases Page,Encl SVP-99-170, Forwards Relief Requests CR-25,CR-26,CR-27,CR-28,PR-11, PR-12 & PR-13,on Basis That Compliance with Specified Requirements Would Result in Hardship or Unusual Difficulty Without Compensating Increase in Level of Quality & Safety1999-08-13013 August 1999 Forwards Relief Requests CR-25,CR-26,CR-27,CR-28,PR-11, PR-12 & PR-13,on Basis That Compliance with Specified Requirements Would Result in Hardship or Unusual Difficulty Without Compensating Increase in Level of Quality & Safety ML20210T9941999-08-13013 August 1999 Forwards Insp Repts 50-254/99-12 & 50-265/99-12 on 990628-0716.Violations Noted SVP-99-154, Notifies NRC That M Price,License SOP-31389,is No Longer Required to Maintain Operator License.Price Was Removed from Licensed Duty on 990729 & Comm Ed Requests License Be Terminated1999-08-13013 August 1999 Notifies NRC That M Price,License SOP-31389,is No Longer Required to Maintain Operator License.Price Was Removed from Licensed Duty on 990729 & Comm Ed Requests License Be Terminated ML20210R9541999-08-10010 August 1999 Informs That During 990804 Telcon Between J Bartlet & M Bielby,Arrangements Were Made for NRC to Insp License Operator Requalification Program at Plant.Insp Planned for Wks of 991018 & 25 ML20210N5651999-08-0606 August 1999 Forwards Rev 8 to Nuclear Generating Stations Emergency Plan, for Plants.With Summary of Changes ML20210M5461999-08-0606 August 1999 Discusses 990804 Telcon Between J Bartlet & M Bielby,Where Arrangements Were Made for NRC to Inspect Licensed Operator Requalification Program at Plant.Insp Planned for Wks of 991018 & 25 ML20210M9131999-08-0202 August 1999 Forwards Response to NRC AL 99-02, Operating Reactor Licensing Action Estimates, for Fys 2000 & 2001 for Comed ML20210L8371999-08-0202 August 1999 Forwards SE Accepting Licensee 60-day Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety Related Motor-Operated Valves ML20210M4691999-07-30030 July 1999 Forwards Insp Repts 50-254/99-14 & 50-265/99-14 on 990713-15.One NCV Was Identified & Discussed in Encl Insp ML20210H4661999-07-29029 July 1999 Forwards Insp Repts 50-254/99-13 & 50-265/99-13 on 990628-0702.No Violations Noted.Insp Consisted of Selective Examination of Procedures & Representative Records, Observations of Activities & Interviews with Personnel 05000254/LER-1999-002, Forwards LER 99-002-01,IAW 10CFR50.73(a)(2)(iv).Rev Includes Cause Codes & Energy Industry Identification Sys Identifiers Which Were Erroneously Omitted in Original Ler.Commitments Listed1999-07-29029 July 1999 Forwards LER 99-002-01,IAW 10CFR50.73(a)(2)(iv).Rev Includes Cause Codes & Energy Industry Identification Sys Identifiers Which Were Erroneously Omitted in Original Ler.Commitments Listed SVP-99-151, Responds to NRC 990701 Telcon RAI Re Licensee Amend Request Re Use of Containment Overpressure to Support NPSH Available for ECCS at Quad Cities Nuclear Power Station,Units 1 & 21999-07-23023 July 1999 Responds to NRC 990701 Telcon RAI Re Licensee Amend Request Re Use of Containment Overpressure to Support NPSH Available for ECCS at Quad Cities Nuclear Power Station,Units 1 & 2 SVP-99-150, Forwards Responses to 990520 RAI Re Annual 10CFR50.46 Rept1999-07-23023 July 1999 Forwards Responses to 990520 RAI Re Annual 10CFR50.46 Rept SVP-99-146, Informs of Termination of License SOP-31132-1,for G Green, as Required by 10CFR50.74(b).Individual Was Removed from License Duty on 9906251999-07-21021 July 1999 Informs of Termination of License SOP-31132-1,for G Green, as Required by 10CFR50.74(b).Individual Was Removed from License Duty on 990625 ML20210B7071999-07-16016 July 1999 Responds to Requesting Review & Approval of Three Proposed Changes to Ceco QA TR,CE-1A Per 10CFR50.54(a)(3) & 10CFR50.4(b)(7) ML20196J9061999-07-0101 July 1999 Provides Evidence That Util Maintains Guarantee of Payment of Deferred Premiums in Amount of $10 Million for Each of Thirteen Reactors,Per 10CFR140.21 ML20196J9131999-07-0101 July 1999 Submits Status of Nuclear Property Insurance Currently Maintained for Braidwood,Byron,Dresden,Lasalle County,Quad Cities & Zion Nuclear Power Stations,Per 10CFR50.54(w)(3) ML20209B8241999-06-30030 June 1999 Forwards Five 3.5 Inch Computer Diskettes Containing Revised Annual Dose Repts for 1994 Through 1998 for Individuals Receiving Neutron Dose Not Previously Included in Reported Total Effective Dose Equivalent Values.Without Diskettes SVP-99-139, Forwards Revised Action 2 & Associated TS Bases Changes, Describing Specific Alternate Method for Determining Drywell Floor Drain Sump Leakage1999-06-30030 June 1999 Forwards Revised Action 2 & Associated TS Bases Changes, Describing Specific Alternate Method for Determining Drywell Floor Drain Sump Leakage ML20209B2081999-06-29029 June 1999 Discusses Closure of Response to RAI Re GL 92-01,Rev 1,Suppl 1, Reactor Vessel Structural Integrity. Rvid,Version 2 Issued as Result of Review of Responses.Info Should Be Reviewed & Comments Submitted by 990901 05000265/LER-1999-002, Forwards LER 99-002-00 for Quad Cities Nuclear Power Station IAW Requirements of 10CFR50.73(a)(2)(i)(B).Util Commits to One Listed Action1999-06-25025 June 1999 Forwards LER 99-002-00 for Quad Cities Nuclear Power Station IAW Requirements of 10CFR50.73(a)(2)(i)(B).Util Commits to One Listed Action SVP-99-122, Forwards Regulatory Commitment Change Summary Rept, Containing Summary Info from 980601 Through 9906011999-06-25025 June 1999 Forwards Regulatory Commitment Change Summary Rept, Containing Summary Info from 980601 Through 990601 SVP-99-066, Informs That J Reed,License SOP-31034-1,was Removed from License Duty in 990618.Termination of License Is Requested1999-06-25025 June 1999 Informs That J Reed,License SOP-31034-1,was Removed from License Duty in 990618.Termination of License Is Requested SVP-99-103, Informs NRC of Results of Subject Evaluation as Committed to in .Evaluation Consisted of Analytically Demonstrating That Cfu Factor for Rv Head Closure Studs Will Remain Below 1.0 for Remainder of Current License Period1999-06-25025 June 1999 Informs NRC of Results of Subject Evaluation as Committed to in .Evaluation Consisted of Analytically Demonstrating That Cfu Factor for Rv Head Closure Studs Will Remain Below 1.0 for Remainder of Current License Period ML20196F7921999-06-24024 June 1999 Forwards Meeting Summary,Nrc Meeting Handout & Licensee Handout from 990608 Meeting ML20196E7131999-06-23023 June 1999 Forwards Insp Repts 50-254/99-09 & 50-265/99-09 on 990421-0531.One Violation of NRC Requirements Occurred & Being Treated as non-cited Violation,Consistent with App C of Enforcement Policy ML20196E4821999-06-21021 June 1999 Discusses 990617 Meeting by Region III Senior Reactor Analysts (SRA) in Cordova,Il to Meet with PRA Staff to Discuss Initiatives in Risk Area & to Establish Dialog Between SRAs & PRA Staff 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARSVP-99-181, Forwards Biennial Update to Quad Cities Ufsar,Iaw 10CFR50.71(e).Update Includes Changes to Facility & Procedures & Are Current Through 9906301999-10-20020 October 1999 Forwards Biennial Update to Quad Cities Ufsar,Iaw 10CFR50.71(e).Update Includes Changes to Facility & Procedures & Are Current Through 990630 ML20217H4661999-10-18018 October 1999 Forwards Changes to EPIPs IAW 10CFR50.54(q) & 10CFR50,App E, Section V.Details of Changes Encl ML20217K7011999-10-13013 October 1999 Provides Response to Questions Related to Request for License Amend,Per 10CFR50.90, Credit for Containment Overpressure. Supporting Calculations Encl 05000254/LER-1999-004, Forwards LER 99-004-00,IAW Requirements of 10CFR50.73(a)(2)(i)(B).Util Is Committed to Listed Action1999-10-12012 October 1999 Forwards LER 99-004-00,IAW Requirements of 10CFR50.73(a)(2)(i)(B).Util Is Committed to Listed Action 05000254/LER-1999-003, Forwards LER 99-003-00 IAW 10CFR73(a)(2)(v)(A).Commitment Made by Util,Listed.Any Other Actions Described in LER Represent Intended or Planned Actions by Licensee1999-10-0707 October 1999 Forwards LER 99-003-00 IAW 10CFR73(a)(2)(v)(A).Commitment Made by Util,Listed.Any Other Actions Described in LER Represent Intended or Planned Actions by Licensee ML20216J8241999-09-30030 September 1999 Notifies of Removal of NRC Headquarters & Region III Offices from Controlled Copy Distribution of Certain CE Documents. Specific Documents,Associated Controlled Copy Numbers & NRC Location Affected Are Shown on Attachment to Ltr SVP-99-189, Confirms Completion of Actions Identified During Review of NRC Safety Evaluation of Boiling Water Reactor Owners Group Rept, Utility Resolution Guidance of ECCS Suction Strainer Blockage1999-09-22022 September 1999 Confirms Completion of Actions Identified During Review of NRC Safety Evaluation of Boiling Water Reactor Owners Group Rept, Utility Resolution Guidance of ECCS Suction Strainer Blockage SVP-99-190, Clarifies Statement Contained in NRC Insp Repts 50-254/99-12 & 50-265/99-12,dtd 990813,paragraph 4OA1.3B, Observation & Findings, Re Sys Mod to DG Air Start Sys1999-09-13013 September 1999 Clarifies Statement Contained in NRC Insp Repts 50-254/99-12 & 50-265/99-12,dtd 990813,paragraph 4OA1.3B, Observation & Findings, Re Sys Mod to DG Air Start Sys ML20211G1221999-08-27027 August 1999 Forwards fitness-for-duty Program Performance Data for Each of Comm Ed Nuclear Power Stations & Corporate Support Employees within Scope of Rule for six-month Period Ending 990630,IAW 10CFR26.71(d) SVP-99-154, Notifies NRC That M Price,License SOP-31389,is No Longer Required to Maintain Operator License.Price Was Removed from Licensed Duty on 990729 & Comm Ed Requests License Be Terminated1999-08-13013 August 1999 Notifies NRC That M Price,License SOP-31389,is No Longer Required to Maintain Operator License.Price Was Removed from Licensed Duty on 990729 & Comm Ed Requests License Be Terminated SVP-99-170, Forwards Relief Requests CR-25,CR-26,CR-27,CR-28,PR-11, PR-12 & PR-13,on Basis That Compliance with Specified Requirements Would Result in Hardship or Unusual Difficulty Without Compensating Increase in Level of Quality & Safety1999-08-13013 August 1999 Forwards Relief Requests CR-25,CR-26,CR-27,CR-28,PR-11, PR-12 & PR-13,on Basis That Compliance with Specified Requirements Would Result in Hardship or Unusual Difficulty Without Compensating Increase in Level of Quality & Safety SVP-99-147, Notifies of Change to Bases of TS to Licenses DPR-29 & DPR- DPR-30.Change to TS Section 3/4.9 Provides Clarity & Consistency with Sys Design Description in Ufsar,Sections 8.3.2.1 & 8.3.2.2.TS Bases Page,Encl1999-08-13013 August 1999 Notifies of Change to Bases of TS to Licenses DPR-29 & DPR- DPR-30.Change to TS Section 3/4.9 Provides Clarity & Consistency with Sys Design Description in Ufsar,Sections 8.3.2.1 & 8.3.2.2.TS Bases Page,Encl ML20210N5651999-08-0606 August 1999 Forwards Rev 8 to Nuclear Generating Stations Emergency Plan, for Plants.With Summary of Changes ML20210M9131999-08-0202 August 1999 Forwards Response to NRC AL 99-02, Operating Reactor Licensing Action Estimates, for Fys 2000 & 2001 for Comed 05000254/LER-1999-002, Forwards LER 99-002-01,IAW 10CFR50.73(a)(2)(iv).Rev Includes Cause Codes & Energy Industry Identification Sys Identifiers Which Were Erroneously Omitted in Original Ler.Commitments Listed1999-07-29029 July 1999 Forwards LER 99-002-01,IAW 10CFR50.73(a)(2)(iv).Rev Includes Cause Codes & Energy Industry Identification Sys Identifiers Which Were Erroneously Omitted in Original Ler.Commitments Listed SVP-99-150, Forwards Responses to 990520 RAI Re Annual 10CFR50.46 Rept1999-07-23023 July 1999 Forwards Responses to 990520 RAI Re Annual 10CFR50.46 Rept SVP-99-151, Responds to NRC 990701 Telcon RAI Re Licensee Amend Request Re Use of Containment Overpressure to Support NPSH Available for ECCS at Quad Cities Nuclear Power Station,Units 1 & 21999-07-23023 July 1999 Responds to NRC 990701 Telcon RAI Re Licensee Amend Request Re Use of Containment Overpressure to Support NPSH Available for ECCS at Quad Cities Nuclear Power Station,Units 1 & 2 SVP-99-146, Informs of Termination of License SOP-31132-1,for G Green, as Required by 10CFR50.74(b).Individual Was Removed from License Duty on 9906251999-07-21021 July 1999 Informs of Termination of License SOP-31132-1,for G Green, as Required by 10CFR50.74(b).Individual Was Removed from License Duty on 990625 ML20196J9061999-07-0101 July 1999 Provides Evidence That Util Maintains Guarantee of Payment of Deferred Premiums in Amount of $10 Million for Each of Thirteen Reactors,Per 10CFR140.21 ML20196J9131999-07-0101 July 1999 Submits Status of Nuclear Property Insurance Currently Maintained for Braidwood,Byron,Dresden,Lasalle County,Quad Cities & Zion Nuclear Power Stations,Per 10CFR50.54(w)(3) ML20209B8241999-06-30030 June 1999 Forwards Five 3.5 Inch Computer Diskettes Containing Revised Annual Dose Repts for 1994 Through 1998 for Individuals Receiving Neutron Dose Not Previously Included in Reported Total Effective Dose Equivalent Values.Without Diskettes SVP-99-139, Forwards Revised Action 2 & Associated TS Bases Changes, Describing Specific Alternate Method for Determining Drywell Floor Drain Sump Leakage1999-06-30030 June 1999 Forwards Revised Action 2 & Associated TS Bases Changes, Describing Specific Alternate Method for Determining Drywell Floor Drain Sump Leakage SVP-99-103, Informs NRC of Results of Subject Evaluation as Committed to in .Evaluation Consisted of Analytically Demonstrating That Cfu Factor for Rv Head Closure Studs Will Remain Below 1.0 for Remainder of Current License Period1999-06-25025 June 1999 Informs NRC of Results of Subject Evaluation as Committed to in .Evaluation Consisted of Analytically Demonstrating That Cfu Factor for Rv Head Closure Studs Will Remain Below 1.0 for Remainder of Current License Period SVP-99-122, Forwards Regulatory Commitment Change Summary Rept, Containing Summary Info from 980601 Through 9906011999-06-25025 June 1999 Forwards Regulatory Commitment Change Summary Rept, Containing Summary Info from 980601 Through 990601 05000265/LER-1999-002, Forwards LER 99-002-00 for Quad Cities Nuclear Power Station IAW Requirements of 10CFR50.73(a)(2)(i)(B).Util Commits to One Listed Action1999-06-25025 June 1999 Forwards LER 99-002-00 for Quad Cities Nuclear Power Station IAW Requirements of 10CFR50.73(a)(2)(i)(B).Util Commits to One Listed Action SVP-99-066, Informs That J Reed,License SOP-31034-1,was Removed from License Duty in 990618.Termination of License Is Requested1999-06-25025 June 1999 Informs That J Reed,License SOP-31034-1,was Removed from License Duty in 990618.Termination of License Is Requested SVP-99-125, Forwards Technical Info Re ECCS Suction Strainers at Quad Cities Nuclear Power Station Units 1 & 2,to Support Review of 990129 Lar.Rev 0 to TR-VQ1500-02, Clean ECCS Suction Strainer Head Loss Test Rept, Encl1999-06-15015 June 1999 Forwards Technical Info Re ECCS Suction Strainers at Quad Cities Nuclear Power Station Units 1 & 2,to Support Review of 990129 Lar.Rev 0 to TR-VQ1500-02, Clean ECCS Suction Strainer Head Loss Test Rept, Encl ML20195E3491999-06-0707 June 1999 Withdraws Util Requesting License Change for Plant Security Plan Rev.Licensee Will re-evaluate Situation & May Request Approval of Change in Future ML20207G1451999-06-0707 June 1999 Forwards Rev 45 to Comed Quad Cities Nuclear Power Station Security Plan.Rev Includes Changes Listed.Security Plan Is Withheld from Public Disclosure Per 10CFR73.21 ML20195D6351999-06-0404 June 1999 Notifies NRC of Actions That Has Been Taken in Accordance with 10CFR26, Fitness for Duty Programs SVP-99-105, Informs NRC of Rev to Schedule for Completing Setpoint/ Uncertainty Calculations & Procedure Changes,Originally Planned for Completion on 9905291999-05-20020 May 1999 Informs NRC of Rev to Schedule for Completing Setpoint/ Uncertainty Calculations & Procedure Changes,Originally Planned for Completion on 990529 ML20195B2301999-05-19019 May 1999 Requests Approval of Proposed Changes to QA Topical Rept CE-1-A,rev 66a.Attachment a Describes Changes,Reason for Change & Basis for Concluding That Revised QAP Incorporating Proposed Changes Continues to Satisfy 10CFR50AppB SVP-99-111, Informs NRC of Current Status of Actions on Response to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design-Basis Accident Conditions1999-05-17017 May 1999 Informs NRC of Current Status of Actions on Response to GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design-Basis Accident Conditions SVP-99-098, Fulfills Thirty Day & Annual Reporting Requirements of 10CFR50.46 for Plant.Eccs Evaluation Change Rept Transmitted in Entirety,Fulfilling Thirty Day & Annual Reporting Requirements Specified in 10CFR50.46(a)(3)(i)1999-05-17017 May 1999 Fulfills Thirty Day & Annual Reporting Requirements of 10CFR50.46 for Plant.Eccs Evaluation Change Rept Transmitted in Entirety,Fulfilling Thirty Day & Annual Reporting Requirements Specified in 10CFR50.46(a)(3)(i) SVP-99-099, Requests Relief from Requirements of 10CFR50.55a(g) Re Submittal of Relief Requests for Those Welds for Which Examinations of Greater than 90% of Weld Vol Was Not Acheived During 2nd ISI Program Interval1999-05-13013 May 1999 Requests Relief from Requirements of 10CFR50.55a(g) Re Submittal of Relief Requests for Those Welds for Which Examinations of Greater than 90% of Weld Vol Was Not Acheived During 2nd ISI Program Interval SVP-99-096, Provides Suppl Response to Violations Noted in Insp Repts 50-254/98-20 & 50-265/98-23.Corrective Actions:Listed Multidiscipline Team Will Perform self-assessment IAW Station Program for self-assessments in May 19991999-05-12012 May 1999 Provides Suppl Response to Violations Noted in Insp Repts 50-254/98-20 & 50-265/98-23.Corrective Actions:Listed Multidiscipline Team Will Perform self-assessment IAW Station Program for self-assessments in May 1999 05000254/LER-1999-001, Forwards LER 99-001-00 for Quad Cities Nuclear Power Station.Licensee Shall Rept Any Operation or Condition Prohibited by Plant Tech Specs.Util Committing to Listed Actions1999-05-12012 May 1999 Forwards LER 99-001-00 for Quad Cities Nuclear Power Station.Licensee Shall Rept Any Operation or Condition Prohibited by Plant Tech Specs.Util Committing to Listed Actions ML20206F5381999-04-30030 April 1999 Forwards Magnetic Tape Containing Annual Dose Repts for 1998 for Braidwood,Byron,Dresden,Lasalle County,Quad Cities & Zion Nuclear Power Stations,Per 10CFR20.2206(c).Without Magnetic Tape SVP-99-108, Forwards Quad Cities 1998 Radiological Environ Operating Rept, IAW Plant TS 6.9.A.3.Rept Contains Results of Radiological Environ & Meteorological Monitoring Programs. Radioactive Effluent Release Rept Was Submitted 9903301999-04-30030 April 1999 Forwards Quad Cities 1998 Radiological Environ Operating Rept, IAW Plant TS 6.9.A.3.Rept Contains Results of Radiological Environ & Meteorological Monitoring Programs. Radioactive Effluent Release Rept Was Submitted 990330 SVP-99-036, Forwards Reg Guide 1.16 Rept Number of Personnel-Rem by Work & Job Function for 1998. Associated Collective Deep Dose Equivalent Reported According to Work & Job Functions1999-04-29029 April 1999 Forwards Reg Guide 1.16 Rept Number of Personnel-Rem by Work & Job Function for 1998. Associated Collective Deep Dose Equivalent Reported According to Work & Job Functions SVP-99-088, Informs That Util Is Withdrawing IST Relief Rquests RV-02B & RV-03B1999-04-29029 April 1999 Informs That Util Is Withdrawing IST Relief Rquests RV-02B & RV-03B ML20205T1141999-04-22022 April 1999 Provides Comments from Technical Review of Draft Info Notice Re Unanticipated Reactor Water Draindown at Quad Cities Nuclear Power Station,Unit 2,ANO,Unit 2 & JAFNPP ML20206B2471999-04-20020 April 1999 Informs That SE Kuczynski Has Been Transferred to Position No Longer Requiring SRO License.Cancel License SOP-31030-1, Effective 990412 SVP-99-065, Requests That License SOP-31516,for Jf Graham,Be Terminated, Per 10CFR50.74(b).Individual Was Removed from License Duty on 990319 & No Longer Requires Operator License1999-04-14014 April 1999 Requests That License SOP-31516,for Jf Graham,Be Terminated, Per 10CFR50.74(b).Individual Was Removed from License Duty on 990319 & No Longer Requires Operator License SVP-99-058, Submits Plant Specific ECCS Evaluation Changes,Per Annual Reporting Requirements of 10CFR50.46.Attachments Include Current Assessment Data Re PCT Info Limiting LOCA Evaluations1999-04-14014 April 1999 Submits Plant Specific ECCS Evaluation Changes,Per Annual Reporting Requirements of 10CFR50.46.Attachments Include Current Assessment Data Re PCT Info Limiting LOCA Evaluations SVP-99-063, Responds to NRC Re Violations Noted in Insp Repts 50-254/98-21 & 50-265/98-21.Corrective Actions:Revised Site ISI Procedure Qcap 0410-06, ISI Plan Implementation for Third Ten Year Insp Interval1999-04-0909 April 1999 Responds to NRC Re Violations Noted in Insp Repts 50-254/98-21 & 50-265/98-21.Corrective Actions:Revised Site ISI Procedure Qcap 0410-06, ISI Plan Implementation for Third Ten Year Insp Interval JAFP-99-0129, Submits Comments on Technical Review of Draft Info Notice Describing Unanticipated Reactor Water Draindown at Quad Cities Unit 2,ANO & FitzPatrick1999-04-0909 April 1999 Submits Comments on Technical Review of Draft Info Notice Describing Unanticipated Reactor Water Draindown at Quad Cities Unit 2,ANO & FitzPatrick SVP-99-057, Notifies of Change to Bases for TSs Section 3/4.5, ECCS, Re1999-04-0505 April 1999 Notifies of Change to Bases for TSs Section 3/4.5, ECCS, Re ML20205K5841999-03-31031 March 1999 Submits Rept on Status of Decommissioning Funding for Reactors Owned by Comm Ed.Attachment 1 Contains Amount of Decommissioning Funds Estimated to Be Required Pursuant to 10CFR50.75(b) & (C) SVP-99-062, Informs NRC of Rev to Schedule for Analytically Demonstrating That Cumulative Usage Factor for Reactor Vessel Head Closure Studs Will Remain Below 1.0 for Remainder of Current License Period1999-03-31031 March 1999 Informs NRC of Rev to Schedule for Analytically Demonstrating That Cumulative Usage Factor for Reactor Vessel Head Closure Studs Will Remain Below 1.0 for Remainder of Current License Period 1999-09-30
[Table view] |
Text
M5TT#F M- "
009 ISbb ~ i
.* ' N) Commonwealth Edison 1400 Oocs Place
[NC '7 4
(d Downers Grove. Illinois 60515 March 6,1994 i
Mr. John B. Martin Regional Administrator U.S. Nuclear Regulatory Commission Region lil 801 Warrenville Road Lisle, IL 60532 4351
Subject:
Quad Cities Nuclear Power Station Unit 1 Request for Regional Enforcement Discretion Regarding Facility Operating License DPR-29, Appendix A, Technical Specification 3.7.D NRC Docket No. 50 254
Reference:
Teleconferences on March 5,1994 between CECO (R. Pleniewicz, et al) and the NRC (B. Clayton, et al) -
Dear Mr. Martin:
This letter documents the results of teleconferences held on March 5,1994, between Commonwealth Edison (CECO) and tha NRC Staff, in which Commonwealth Edison requested a Notice of Enforcement Discretion from Technical Specification 3.7.D for Quad Cities Unit 1.
On March 4,1994, Quad Cities declared the inboard isolation valve on the Reactor Core isolation Cooling (RCIC) system (MO 1 1301 16) inoperable due to the results of an EPRI test concerning the valve f actor. In accordance with Technical Specification 3.7.D, the outboard isolation valve on the RCIC steam supply line (MO 1-1301-17) was closed, rendering RCIC inoperable, and placing the station in a 14-day time clock (Technical Specification 3.5.E).
In the referenced teleconferences, CECc requested that Quad Cities Unit I be allowed to operate with the inboard and outboard isolation valves on the RCIC steam supply line open, and the inboard isolation valve inoperable. This would allow RCIC to be i operable and available for accident mitigation. A Notice of Enforcement Discretion was verbally approved by Region 111 on March 5,1994, during the referenced teleconferences.
The basis of the request is provided in Attachment 1 and includes:
- The Technical Specification for which a Notice of Enforcement Discretion is requested:
- The circumstances surrounding the condition, including the need for prompt action; 9409280158 940306 i PDR P
ADOCK 05000234 PDR .
M I i
Mr. J.B. Martin March 6,1994
- The safety basis for the request that enforcement discretion be exercised, including an evaluation of the safety significance and potential consequences of the proposed course of action; The proposed compensatory measures;
- The justification for the duration of the request;
- The basis for the conclusion that the request w0l not have a potential adverse impact on the public health and safety end that a significant safety hazard is not involved;
- The basis for the conclusion.that the request will not involve adverse consequences to the environment.
CECO will shut down Quad Cities Station Unit 1 on March 13,1994 for the start of the 13th refuel outage. During that outage, the valve will be made operable.
This request does not affect Unit 2, as the HPCI and RCIC steem supply valves on that unit, as well as the HPCI valves and outboard isolation valve on RCIC for Unit 1, have been shown to be operable.
This request for Enforcement Discretion has been reviewed and approved by the Quad Cities Station Plant Operations Review Committee per station policy and procedure.
CECO appreciates the NRC staff's effort and participation in the review of this request. Please direct any questions or comments to John Schrage, Nuclear Licensing Administrator, at (708) 683 7283.
Very truly yours r John L. hre e i ar Licensing Administrator I Attachment cc: Document Control Desk - NRC Docket No. 50 264 B. Clayton, Branch Chief - Region ill C. Miller, Senior Resident inspector - Quod Cities j C. Patel, Project Manager - NRR l Office of Nuclear Facility Safety - IDNS 4
_g . - _ - -
g, I- '
l l REQUEST FOR ENFORCEMENT DISCRETION l.
QUAD CITIES STATION UNIT 1 MARCH 6,1994
- 1. TECHNICAL SPEC 6FICATION OR UCENSING CONDITION WHICH REQUIRES j ENFORCEMENT DISCRETION l
Technical Specification Section 3.7.D provides the requirements for Primary Containment isolation Valves. Specification 3.7.D.1 requires that during power operating conditions, all isolation valves listed in Table 3.7-1 which contact the primary coolant system be operable except as specified in Specification 3.7.D.2.
Specification 3.7.D.2 allows for continued power operation in the event any isolation valves specified in Table 3.7-1 become Inoperable provided that at least '
I one valve in each line having an inoperable valve is in the mode corresponding to the isolated condition. Specification 3.7.D.3 requires the initiation of an orderly shutdown of the reactor, in order to achieve the cold shutdown condition within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, if Specifications 3.7.D.1 and 3.7.D.2 cannot be met.
1 On March 4,1994, Commonwealth Edison Company (CECol determined that the Reactor Core isolation Cooling (RCIC) steam line inboard isolation valve, MO 1- 1 1301-16, would not perform its required design isolation function. As a result, the !
outboard isolation valve, MO 1-1301-17. was placed in the isolated condition ,
(closed) in accordance with Specification 3.7.D.2, and the Unit 1 RCIC System was declared inoperable. In order to restore the availability of RCIC until the upcoming ,
l t Unit I refueling outage (Q1R13), which is scheduled to commence on March 13, ,
l 1994, CECO is requesting Enforcement Discretion from Technical Specification i Section 3.7.0 for MO 1-1301-16, for one time only, until March 13,1994. This !
Enforcement Discretion wiV Niow the reopening of the MO 1-1301-17 valve, and l thus restore the availability o' he Unit 1 RCIC System. ;
! 2. CIRCUMSTANCES SURROUNDING THE SITUATION On December 12,1993, the NRC issued Information Notice 93-88, " Status of Motor-Operated Valve Performance Prediction Program by the Electric Power :
Research Institute," which described EPRl's performance prediction testing program i for MOVs and presented some preliminary results. The preliminary EPRI results were received by CECO at an industry meeting in Delles, Texas on December 1, l 1993. On December 14,1993, EPRI issued the formal test results, specifications, i and drawings for EPRI flow loop tested valves to the utilities which sponsored the i I
testing. CECO began evaluating the test results for applicability. The CECO evaluation encompassed discussions with Crane and EPRI to determ*me which blowdown valves were similar to the EPRI-tested 6" Crane velves. At Quad Cities, those valves were determined to be the 1(2) 1301-18 & 17 (RCIC Steam Line isolation) and the 1(2).2301-4 & 5 (HPCI Steam Line Isolation), which are Crane
~
carbon steel 783U gate valves.
On March 3,1994, results from the vendor and EPRI feedback were evaluated by corporate and site engineering, On the basis of this evaluation, all Crane carbon steel 783U blowdown valves were determined to be susceptible to the damage
m; gp g y.gf ; yg;pg . a ugatar.v vrr-mechanism identified by the EPRI testing. An operability evatuation was initleted,
'and it was concluded that the MO 1 1301-16 valve was inoperable (on 3/4/94). All '
other susceptible blowdown valves (2-1301 16,1(2)-1301-17, and 1(21-23014 &
- 5) were determined to be operable. ,
Currently, the Unit 1 RCIC System is inoperable, with the MO 1-1301 17 vs. ;
closed. Prompt action is necessary to io establish the operability of the RCIC system during operation of Unit 1 until March 13,1994.
- 3. EVALUATION OF SAFETY SIGNIFICANCE AND CONSEQUENCES The RCIC Steam Supply Containment Isolation valves (see attached Figure, " Quod Cities 1 Reactos Core isolation Cooling System") have the following safety functions:
- They form part of the reactor coolant pressure boundary.
- They isolate ths RCIC steam line, and therefore the reactor vessel, in case of a line break in the RCIC steam line.
MO 1-1301 16 is capable of isolating the steem line at a maximum dP of 1084 psid. The valve is required to close across a maximum dP of 1146 psid.
MO 1-1301-17 is capable of isolating the steam line in the event of a RCIC steam line break at a dP of 1146 paid. This valve receives an isolation signal at the same time as MO 1 1301 16. Assuming that both volves have power to close, the total differential pressure between the reactor and the break would be shared across the two valves. The reduced pressure load will increase the likelihood of MO 1 1301-16 closing.
PROBABILITY RISK ASSESSMENT REVIEW A coro damage frequency comparison between leaving RCIC inoperable and having a RCIC steam line break without isolation was performed. The result of this evaluation was that the estimated core damage frequency increase for having RCIC inoperable was 24 times higher than for the RCIC steam line rupture without isolation. CECO has concluded that the plant would be in a sofer condition by opening MO 1 1301-17.
LIKELlHOOD OF A LINE BREAK l There is a probability of 4.4x104that the RCIC steam line will break in the next nine days. This is based on a piping failure rate of 8.6x10'"/Hr-section with 20 piping sections in this line, plus a valve failure rate of 1.5x10/Hr component with 2 valves in the line.
Additionally, as described in the CECO Safety Assessment submitted l' . *oonse to Generic Letter 89-10 Supplement 3 (D. Taylor to USNRC letter dated Mk. ;n 11, 2-
{
l l
1
~ 7JWEbEWW
~
bi- g. 'g- g-gg :~g: E m - -
1991), the Leak Before Break (LBB) concept is based on the f act that reactor piping is f abricated from tough ductile materials which can tolerate large through-wall cracks without fracture under service loadings. By monitoring the leak rate from through-wall cracks and setting conservative limits on the leakage, cracks in piping can be detected well before the margin to rupture is challenged.
In NUREG 1061, Volume 3, the NRC Piping Review Committee outlined the limitations and general technical guidance on LBB analysis to justify mechanistically that breaks in high-energy fluid system piping need not be postulated, in General Design Criterion (GDC) 4, the NRC has formalized the use of the LBB approach to justify the elimination of pipe-whip restraint and jet impingement barriers as design I requirements for hypothetical Double Ended Guillotine Break (DEGB) in high snergy '
reactor piping systems.
As detailed in the GL 89-10, Supplement 3 Safety Assessment, the LBB approach is used to illustrate the concept of detecting and mitigating leakage prior to a pipe rupture. Leakage from a through-wall crack with a length up to, but less than, the critical crack length would be large enough to be readily detected. Thus isolations '
can be achieved well before the crack grows to critical length and well below the point where design basis flows and pressures are established.
Based on the evaluation results,it is concluded that the RCIC steam supply line is expected to develop a detectable leak prior to reaching the point of incipient break.
Thus, a DEGB in these lines is highly unlikely.
The crack and leak will be detected prior to the DEGB. This allows sufficient time for the RCIC isolation valves to be closed prior to a condition developing that would create a dP greater than 1084 psid. In this event either the MO 1 1301-16 or the MO 1 1301 17 valve will close.
EFFECTS OF A RCIC LINE BREAK ll the RCIC Room tamperature is raised to the high temperature isolation setting l (170*F), or if the RCIC steam line reaches 300% flow, MO 1130116 and MO 1- l 1301-17 will receive a signal to isolate and a control room annunciator will alarm. l If this line breaks in the drywell, the containment isolation valves will close since the differential pressure across the valves would be less than 1084 psid. The effects of this event would be bounded by the recirculation line break accident scenario described in the FSAR.
Realistically, there may exist an obstruction from the downstream piping system if the line break was not a guillotine type break. This obstruction may reduce the differential pressure across the valve. If the line break does not occur at the valve, the affects of pipe elbows and line losses may also lower the differential pressure across the isolation valve. A reduced differential pressure across the valve will require less thrust for valve closure during a line break event.
3-
E l BY: 3- b-34 ; U:23t'M : -
443 7601:: 7/.
b
- The steam flow out the RCIC line break is reduced in proportion to the reactor pressure during depressurization. After full reactor depressurization, steem flow is i I
! assumed to be minimal. Therefore, inventory loss will be terminated after full depressurization.
1 This break scenario is anticipated to result in liquid inventory losses less than the design basis MSLB event. This break would occur inside the secondary l j
containment, with additional removal of radionuclides accomplished by the Standby Gas Treatment (SBGT) System, as well es deposition within the reactor bu Iding.
Therefore this scenario does not present unacceptable consequences beyond previously licensed events.
The water necessary to makeup the inventory loss for this Loss of Coolant Accident (LOCA) is well within the capabilities of the station's water storage systems. The two condensate storage tanks haw a capacity of 500,000 gallons. The HPCI suction is normally from these tanks. The low pressure ECCS pumps can draw suction from the Torus (1,000,000 gallons) that can also restore the lost reactor coolant inventory.
The RCIC isolation valves are qualified for the harsh environment that would be 1
created by a guillotine rupture. The ECCS pumps and motors are qualified to a steam environment and are expected to perform their design functions in the event i of a line break.
The divisional zed ECCS equipment is located in rooms adjacent to the Torus. The walls of these rooms are flood barriers equipped with submarine doors. The motors for the pumps are elevated so that flooding in the Individual rooms will not necessarily render the equipment inoperable. The ECCS equipment rooms all communicate with the Torus area through pipe chases. These wall openings are located above the maximum flood height. Emergency Operating Procedures for Secondary Containment control provide for mitigation of flooding. The Torus basement sumps will receive a high level alarm, which may provide useful information to the control room operator. These sumps isolate on low reactor water level, high drywell pressure or high drywell radiation. In summary, the existing flood protection features are expected to maintain the ECCS equipment operable
) during and after the line break event.
The release of large quantities of steam to the reactor building will result in an
, l increase to on-site dose. However,it is postulated that most of the release will be I confined to the reactor building and processed by Redweste and SBGT. Area Radiation Monitors would alert the operators and personnel that radiological conditions were changing.
i The on site dose consequences of a line break are expected to be less severe than a Main Steam Line break (MSLB) scenario, which releases large quantities of steam to the turbine building. A turbine building release in expected to have a greater effect
, on control room doses than the unisolebte RCIC steam line break.
J The quantities of steam released by the postulated unisolable RCIC steam line breaks are less than or equal to that postulated for a MSLB scenario. Ihis scenario, 4
1
D M; U- 7-34 :1U;U7AN . _. 443 7obl;; 2/ l
.which is evaluated in the FSAR, results in a release well below the limits of 10 C
- 100. Therefore, the unisolable RCIC line break will not result in off site doses in excess of 10 CFR 100 limits, in the un!ikely event of an unisolable pipe break, the operators, following the direction provided in the Emergency Operating Procedures, would SCRAM the unit and depressurize the vessel. This action would minimize the force driving reactor coolant out the line break. Any emergency core cooling pump is capable of restoring the lost reactor coolant inventory. The ECCS pumps are environmentally qualified and protected by flood barriers. A line break of the RCIC system is bounded by the release due to the Main Steam Une Broek described in the FSAR.
The MSLB at full power resutts in 40% of the allowable values of 10 CFR 100. l Therefore, the on-site and off site dose consequences of an unisolable RCIC pipe ;
break will be below the requirements of 10 CFR 100.
- 4. COMPENSATORY ACTIONS Compensatory measures, as indicated below, will be implemented to support t request fe Enforcement Discretion:
The operating crews will be briefed on this issue as they come on shift.
1-1301-17 and MO 1-They will be given direction to attempt to close MO 1301 61 in the event of an1 unisolated RCIC steam line break. This may 1301-18 enough to allow the valve to isolate tho reduce the dP across MO break. In the event the line can not be isolated, the operators have guidanct l
in the Emergency Operating Procadures to depressurize the reactor when an l area reaches Maximum Safe Operaung Temperature or Radiation level.
A caution card will be placed on the control switch for the RCIC inboard steam supply isolation valve, explaining that the valve may not close during a full dP blowdown through a break in the RCIC ateam supply line.
No unnecessary preventative maintenance or system outages will be performed.
No work that increases the potential for a line break will be performed.
l
- 5. JUSTIFICATION FOR THE DURATION OF THE REQUEST !
13,1994, at The requested duration for the enf orcement discretion is until March 1.
which time Unit 1 is scheduled to shutdown for the 13th refueling outtge (01R12 This timeframe is justified by the following items:
The power provided by Unit 1 will be important to the Ceco system during' the next week. The Commonwealth Edison Company has six cool and fou
~
nuclear units down next week.
.s.
esw en r u9fi TEL~UTag
~
~ 460 Tool W c/;
Compounding the situaticn is the fact that a railrsed strike has reduced the quantity of coal to the Midwest (inventories at all of CECO's coal Stations
- are quite low). There presently exists a court injunction to helt the strike; however restoration of coalinventories is not assured.
Iowa Illinois Gas and Electric is also in a coal conservation mode, due to the ;
strike, and has shut down the Louisa plant. This strike end the potential for flooding of the Mississippi River have compounded their coal delivery problems and forced the utility to curtail electric generation.
i Repair of the MO 1-1301 16 would require a plant shutdown, and would not ]
be completed prior to the refuel outage. Although work on this valve was :
planned for the refuel outage, this work scope will be enhanced to assure l 1
valve operability after the refuel outage.
The likelihood of a break in the steam supply piping for the RCIC system .
occurring during the requested time frame is extremely low. l
- 6. EVALUATION OF SIGNIFICANT HAZARDS CONSIDERATION Commonwealth Edison has evaluated this request for Discretionary Enforcement and determined that it does not represent a significant hazards consideration.
Based on the criteria for defining a significant hazards consiueration established in 10 CFR 50.g2, operation of Quad Cities Station Unit 1 in accordance with the proposed request will not:
Involve a significant increase in the probability or consequences of an sccident previously evaluated because:
j
) The proposed request will allow operation of Unit 1 with the inboard RCIC
! steam supply valve open and inoperable, while the outboard isolation valve i t i open and operable. This does not change the probability of any previously analyzed accident, nor does it significantly increase the consequences of a j previously analyzed accidert, l The steam supply isolation valve for RCIC does not affect any accident i precursors or initiators, and therefore, does not affect the probability of a i previously analyzed accident.
i The consequences of a steam line break on the RCIC system are not j significantly increased because of the items noted in section 3, and listed j below.
a) There is a high likelihood that the pipe will ieak such that it en n be isolated before it breaks; i
! b) There is a limited likelihood for the occurrones of a break in tm L RCIC steam supply line outside containment during the short i time frame for which the request is being made; l
l 6-1
5t31 !$Y : U- 7-34 ;10;UoAM . -
443 7 eel:= 4f .
l l
1 c) There in a high likelihood that the break will not be a full
'. guillotine rupture; l d) The radiological affects and inventory loss are bounded by the MSLB analysis. The on site and off site dose consequences of the MSLB are below 10 CFR 100 limits;
~
e) There is a high likelihood that the opereble outboard valve will close, isolating the line. This will decrease the differential ,
pressure that the inboard valve will have to close against.
The radiological consequences of a steam supply line break on the RCIC system are not significantly increased, as supported by the items listed above. Therefore, the consequences of a previously analyzed accident are not significantly increased.
Create the possibility of a new or different kind of accident from any accident previously evaluated because:
The proposed request will allow operation of Unit 1 with the inboard RCIC steam supply valve open and inoperable, while the outboard isolation valve is open and operable. This will allow RCIC to be operable and availabla for accident mitigation. A steam line break is an analyzed accident. This mode of operation does not create the possibiftty of a new or different kind of accident.
Involve a significant reduction in the margin of safety because:
Allowing the Unit to be operated with an open and inoperable RCIC steam supply valve does not significantly reduce the margin of safety. The low likelihood of a steam line break during the short time frame for which the request is being rnsde, the high likelihood of identifying a leak with tims to isolate the leak, the high likelihood that the other isetation valve will operate as designed (and the positive effect this may have on the ability of the inboard valve to operate), and the bounding analysis for the MSL break, support that the margin to 10 CFR 100 limits as a result of having one inoperable RCIC steam supply valve for the time period requested, and with the noted compensatory actions in place, is not significantly reduced.
- 7. ENVIRONMENTAL ASSESSMEffr Commonwealth Edison has evaluated the proposed discretionary enforcement request against the criteria for the identification of licensing and regulatory actions requiring an environmental essessment in accordance with 10 CFR 51.21. It has been determined that the proposed change meets the criteria for a categorical exclusion as provided in 10 CFR 51.22(c)(9). This conclusion has been determineo because the proposed changes do not pose a significant hazards consideration and do not involve a significant increase in the amounts or changes in the types of effluents released offsite. The proposed change does not involve a significant increase in individual or cumulative occupational radiation exposure. The quantitie s 7
4
of steem released by the postulated unisolable RCIC steem line breaks are less than
.or aquel to that postulated for a MSLB scenario. This scenario, which is evaluated
- in the FSAR, results in a release well below the limits of 10 CFR 100. Therefore, the unisolable RCIC line break will not result in off site doses in excess of 10 CFR 100 limits.
- 8. APPROVAL BY STATION REVIEW Tha request has been reviewed and approved by the Plant Operating Review Committee.
8-t 1
G 4
6 r 1
% i; s t u a i !
i i 1 5 f"""1 O lk' Oa l
. s u ilMO A I I i '
8 k
- Z}
!io iXs IE!
-k, I jl II: E0 i
q "i"
-[ill 1x.
3t
!Io tb , o Ao k
- i .. i I' Gs E 1 x
g i-I-T EX iX+ l o al]EO il] [O E %8
- i
.T 1RXO -
i E
8 o
8 siX sp '
IR:EO II !;g i ;F_s i sk4 "
$. i ih IV+
46 <>
"N _
I 1 l
- li )5
! IX5 1
)
il i gg[g I[g M I I i i i$o it