ML20010F746

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LER 81-132/03L-0:on 810806,unidentified Leakage Exceeding 1 Gpm Was Identified During Testing of RCS Water Inventory Balance.Caused by Several Vent & Drain Valves on RCS Leaking.Valves & Pipe Caps Tightened Down
ML20010F746
Person / Time
Site: McGuire Duke Energy icon.png
Issue date: 09/02/1981
From: Nardoci P
DUKE POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20010F744 List:
References
LER-81-132-03L, LER-81-132-3L, NUDOCS 8109110277
Download: ML20010F746 (1)


Text

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i a i 2 4 I While in Mode 3, performance of a reactor coolant system water inventory bal- ,

,,,3 gance by a periodic test (reactor coolant leakag2 calculation) indicated that i2..i ithe unidentified leakage exceeded .1 GPM (1.154 GPM). This violates T.S.3.4.7.2,

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! o e s ! f the reactor buildinc. the water would have gone to the containment sump and ,

93,,i 9 then be pumped to tanks in the plant waste systems for processing. Thus, the

, health and safety of the public were not affected.

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,,,,,;Sec{ral vent and drain valves on the reactor coolant system were discovered to,

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g ,the reactor coolant leakage calculation was run successfully with the unidentiT i,.:6f fied leakage less than 1 GPM ( 0.741 GPM) .  ;

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