ML17311A588

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Insp Repts 50-528/94-34,50-529/94-34 & 50-530/94-34 on 941016-1130.Deviations Noted.Major Areas Inspected:Plant Status,Onsite Response to Events,Operational Safety Verification & Maint Observation
ML17311A588
Person / Time
Site: Palo Verde  Arizona Public Service icon.png
Issue date: 01/10/1995
From: Wong H
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML17311A585 List:
References
50-528-94-34, 50-529-94-34, 50-530-94-34, NUDOCS 9501240405
Download: ML17311A588 (56)


See also: IR 05000528/1994034

Text

APPENDIX B

U.S.

NUCLEAR REGULATORY COMMISSION

REGION IV

Inspection

Report:

50-528/94-34

50-529/94-34

50-530/94-34

Licenses:

NPF-41

NPF-51

NPF-74

Licensee:

Arizona Public Service

Company

P.O.

Box 53999

Phoenix,

Arizona

Facility Name:

Palo Verde Nuclear Generating Station,

Units 1, 2,

and

3

Inspection At:

Maricopa County,

Tonopah,

AZ

Inspection

Conducted:

October

16 through

November 30,

1994

Inspectors:

K. Johnston,

Senior Resident

Inspector

H. Freeman,

Resident

Inspector

A. MacDougall, Resident

Inspector

J.

Kramer, Resident

Inspector

Approved:

. J.

Wong,

C

,

eact

roJects

Branc

lo

ate

Ins ection

Summar

Areas

Ins ected

Units

1

2

and

3

Routine,

announced

inspection of plant

status,-onsite

response

to events,

operational

safety verification,

maintenance

observations,

onsite engineering,

plant support activities,

operations,

maintenance,

and engineering

followup, and licensee

event report

review.

In addition, TI 2515/126 concerning

the performance of online

maintenance

was performed.

Results

Units

1

2

and

3

0 erations

Conduct of operations

weaknesses

contributed to significant operator errors

involving balance of plant equipment during the Unit 2 restart following a

midcycle outage

(Section 2.2).

Licensee

management

took aggressive

actions to

address

these

weaknesses

by revising crew expectations,

reassigning

crew

leaders,

and making significant organization

changes

(Section 3.4).

9501240405 950fi7

PDR

ADOCK 05000528

PDR

I'<

il',

tl

Operations

management

made appropriate operability determinations

regarding

the erratic behavior of the pressurizer

head vent valves

and ultimately shut

down Unit

1 to repair the valves

(Section 3.6).

Additionally, operations

management

responded

appropriately to minor weaknesses

identified by

inspectors

in the application of temporary

procedure

changes

(special

variances,

Section 3.5), with the consistent

positioning of control rod

automatic controls

(Section 3.3)

and with the procedure

governing

independent

verifications (Section

2. 1. 1).

However, operations

management

was slow to

assess

the Technical Specification

(TS) implications of the failure of a

Unit

2 safety injection valve to operate

and communicate

these

implications to

the other two units (Section

2. 1.2).

The

NRC inspector's

identification of switched

lamp covers

on

a remote

shutdown

panel

in Unit 2 highlighted the need for operators

to be alert for

discrepant

conditions

(Section 3. 1).

Maintenance

'While most maintenance

activities observed

during the period were performed

satisfactorily,

the inspectors

found that

a weak procedure

was

used to perform

significant work on pressurizer vent'alves

even though these

procedure

weaknesses

had

been previously identified (Section 4).

The licensee

did not adequately

implement commitments'involving the control of

maintenance activities with an impact

on vital

DC power systems

in Unit 2 and

in the switchyard.

In'hree instances,

work in these

areas

was not adequately

controlled (Section 3.2).

The licensee

has

demonstrated

a carefully considered

approach

to the

performance of online maintenance

on risk significant equipment.

Additionally, enhancements

were planned to improve the ability for operations

and maintenance

personnel

to assess

the risk significance of emergent

work

(Section 7).

En ineerin

Engineering

provided strong support

and analyses

of the spent fuel pool

shuffle (Section

6. 1),

a

10 CFR Part 21 regarding certain motor-operated

valves '(MOV) (Section

2. 1.3),

and the risk assessment

for online maintenance

activities (Section 7).

However, they did not ensure that design

assumptions

for certain safety injection valves were adequately

communicated

to plant

operations

or factored into operating

procedures

and practice

(Section

2. 1.2).

Plant

Su

ort

Inspectors

observed

a successful

emergency

preparedness

drill in which the

licensee

demonstrated

good communications

between

the simulator, technical

support center,

and the emergency

operations facility (Section 5).

I

f

"I

Security took appropriate

actions

in response

to an access

badge left in a

locker

and

a degraded

access turnstile (Section 8).

Hang ement Overview

Hanagement's

efforts in the area of operations'xpectations

and changes

in

the crew staffing and organization

demonstrated

an understanding

of conduct of

operations'eaknesses.

The findings concerning

the implementation of commitments

on the control of

maintenance

on Unit 2 125-Vdc power

systems

and access

to the switchyard,

shortly after those

commitments

were made,

indicated that management

had not

adequately

communicated

these

commitments to site personnel.

Summar

of Ins ection Findin s:

~

Two unresolved

items were identified involving the failure of a Unit 2

safety injection valve to open during testing

(Section

2. 1.2)

and the

adequacy of maintenance

instructions for solenoid operated

valves

(Section 4.1).

~

One deviation

was identified involving three instances

where the

licensee

did not meet

commitments

made to control Unit 2 maintenance

activities involving 125-Vdc equipment,

and in the switchyard

(Section 3.2).

~

TI 2515/126 concerning

the performance of online maintenance

was

performed

(Section 7),

~

Violations 528/9422-01

and 530/9420-01

were closed.

~

Followup items 528/9355-02,

529/9402-02,

and 528/9348-04

were closed.

~

Licensee

Event Reports

528/94-05,

Revision

1, 529/91-05,

529/94-02,

530/94-05,

530/94-06,

and 530/94-07

were closed.

Attachments:

~

Attachment

A - Persons

Contacted

and Exit Heeting

~

Attachment

8 - List of Acronyms

I'

I

e

1

PLANT STATUS

1.1

Unit

1

Unit

1 operated

at 98 percent

power for most of the inspection period.

On

November

26,

1994,

the unit commenced

.a shutdown required

by the plant

TS to

repair two leaking pressurizer

steam

space

vent valves

(Section 3.6).

The

valves

were repaired

in Mode

4 and the reactor

was brought critical on

November 28.

The main generator

breakers

were closed

on November 30.

At the

end of the inspection period, reactor

power was

18 percent

and being raised to

98 percent.

1.2

Unit 2

Unit

2 began the inspection period in Mode

3 preparing for reactor startup

after completing

a midcycle outage for steam generator

tube inspections.

On

October

16,

1994,

the reactor

was

made critical and entered

Mode 1.

1

On October

17, the unit was placed

on the grid and

power raised to

19 percent.

The feedwater

system failed to swap over from the downcomer to the economizer

and power was reduced

to

15 percent to allow repairs.

The licensee

tripped

the turbine after

an operator error resulted

in a main feedwater

pump trip

(Section 2.2. 1),

and the reactor

was stabilized in Mode

2 at approximately

two

percent

power.

On October

19, the licensee

manually tripped the reactor

and entered

Mode

3

when they were unable to restore

a safety injection valve within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />

after it failed to open during testing

on October

16 (Section

2. 1).

The

following day, after completion of the valve repairs,

the unit was taken

critical, placed

on the grid,

and

began

power ascension

to

100 percent.

On October

29, the unit sustained

a reactor trip as

a result of a protection

system

equipment failure (Section 2).

On October 30, the licensee

completed

the equipment repairs

and the unit was taken critical.

On October 31, the

unit entered

Mode 1, placed

on the grid,

and

began

power ascension

to 100

percent

power.

The unit remained at essentially

100 percent

power through the

remainder of the inspection period.

1.3

Unit 3

Unit 3 began

the inspection period

and remained at essentially

100 percent

power until the unit began

a planned

downpower

on November 25.

The unit ended

the inspection period in Mode

5 conducting

a midcycle outage for steam

generator

tube inspections.

2

ONSITE RESPONSE

TO

EVENTS (93702)

2. 1

Unit 2 Hi

h Pressure

Safet

In ection Valve

HPSI

Failed to 0 en Durin

~Testin

On October

15,

1994, Unit 2 conducted

a plant heatup to normal operating

temperature

and pressure.

During the heatup,

operators

received

a 'safety

injection (SI) check valve high pressure

alarm and noted that the pressure

was

above the alarm setpoint of 1000 psig.

This alarm indicated that the check

valve between

the reactor coolant system

(RCS)

and the SI line to

RCS Loop 2B

was leaking..

The following day,

a HPSI isolation valve,

two check valves

upstream of the line which had the high pressure

alarm, failed to open during

testing.

The initial investigation determined that the

HPSI valve

may have

failed due to pressure

binding.

The inspector

reviewed the following:

~

the operators

response

to the high pressure

alarm,

~

the licensee's

review of the failure of the

HPSI valve to open,

and

~

a

10 CFR Part 21 notification regarding

pressure

binding in HPSI valves

similar in design to the one that failed to open.

2. 1. 1

SI Line High Pressure

Alarm

On October

15, operators

in Unit 2 received

a SI check valve high pressure

alarm.

They noted that the pressure

was

above the alarm setpoint of 1000 psig

and determined that reactor coolant

Loop 2B had

a leaking check valve.

The

operators

determined that the leakage

was less

than the

one

gpm TS limit and

attempted

to lower the pressure

and clear the alarm in accordance

with the

annunciator

response

procedure

(ARP).

The

ARP had

a step to open Valve SIB-628, the SI line to

RCS

Loop

2B drain

valve, to lower the pressure

and clear the alarm.

The inspector

noted that

applicable

procedures

seemed

to indicate that operators

should

be performing

an independent verification

( IV) of valve position every time drain Valve SIB-

628 was closed.

However,

the inspector

noted that while operators

opened

and

closed

Valve SIB-628 at least

ten times,

they performed

an

IV only the final

time the valve was closed.

The

ARP referenced

a procedure

governing

IYs for guidance

on when to perform

an IV.

The IV procedure

stated that

an

IV was not needed for control

board

manipulations with valve position indication (as

was the case with

Valve SIB-628) unless directed

by another

procedure.

While this apparent

logic loop provided confusion,

operators

met the intent of the IV procedure.

The licensee

determined that documenting

the

IV of valves operated

from the

control

room was not required

because

valve position indication was

/

0

continuously available.

The licensee

agreed that the

IV procedure

was poorly

written and subject to interpretation

and planned to revise the procedure.

The Unit 2 Operations

Department

leader also wrote

a night order to all three

units discussing this issue

and providing examples

on

how to properly perform

IVs.

As

a long term action,

the licensee

planned to review other operations

procedures

arid remove references

to the

IV procedure for valves operated

from

the control

room.

The inspector

concluded that these

actions

were

'ppropriate.

2'.2

HPSI Valve Failed

To Open

On October

16,

1994, Unit 2 HPSI Valve SIA-UV-627- failed to open during

a

routine

ASME Section

XI stroke test,

Unit

2 had just entered

Mode

1 following

a midcycle outage

when operators

performed the test.

Valve SIA-UV-627 is one

of eight

HPSI injection valves that opens

in conjunction with a HPSI

pump

actuation,

The licensee

decided to replace

the motor operator

on Valve SIA-UY-627 with a

'larger operator

in accordance

with an existing design modification package.

Additionally, th'ey replaced

the valve internals.

They were unable to complete

the repairs within the

72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> allowed outage

time and shutdown Unit 2 on

October

19.

Repairs

were completed,

and the Unit 2 returned to Mode

1 on

October

20.

The licensee

postulated

that Valve SIA-UV-627 may have

been pressure

bound.

Two of the three

check valves

between

the valve

and the

RCS were

known to have

been leaking.

As noted in Section

2. 1. 1, operators

had identified that

a

pressure

indicator at the discharge of the associated

SI tank (SIT), two check

valves

downstream of Valve SIA-UV-627, was reading at

RCS pressure

(roughly

2250 psig).

Licensee

valve engineers

noted that their calculations

supporting the operator

size for Valve SIA-UV-627 were based

on

a maximum differential pressure

across

the valve of 1050 psig.

The maximum differential pressure

had

been

based

on

a

high pressure

alarm of 1000 psig

on the pressure

indicator at the discharge of

the SIT.

On October

21, the inspector

noted that operators

in Units

1 and

3 were

.unaware of the problems with Valve SIA-UV-627 in Unit 2 and were not aware

that

a pressure

of greater

than

1000 psig at the SIT discharge

could imply

that the

HPSI injection valves might not open.

The inspector questioned

whether

an indication of greater

than

1000 psig would require operators

to

enter

TS 3.0.3 since the indication would apply to both

A and

B train HPSI

injection valves associated

with one cold leg injection path.

Operations

management

concurred that, until

an engineering

evaluation could

be completed,

this would be appropriate

and revised

the

ARP for downstream

pressure

alarms

requiring entry into TS 3.0,3

and actions to bleed pressure off the line.

The licensee

issued

Licensee

Event Report

(LER) 529/94-05

on November

18,

1994

describing

the plant shutdown required

by the

TS.

The

LER indicated that

a

0

0

ropt cause

investigation

was underway to determine if Valve SIA-UV-627 was

pressure

bound.

The licensee

planned testing involving a mockup of the

components

that were removed.

Additionally, the licensee

informed the

inspector that they were investigating the following:

~

If the cause

was pressure

binding,

was the

HPSI injection line. for Cold

Leg

2B inoperable while downstream

pressure

was

above

1050 psig?

The

licensee

speculated

that the coincident

HPSI

pump start could have

reduced differential pressure

prior to the injection valve operators

failing.

Why was the basis for Valve SIA-UV-627 not fully communicated

to

operations?

If the valve engineers

assumed

that downstream

pressure

-should

be less

than 3050 psig,

why was this not adequately

communicated

to operations?

~

Are there other

HOVs in which operations

assumptions

were made,

but not

adequately

communicated?

Based

on these

questions,

the inspector

considered

this to be

an Unresolved

Item (529/9434-01).

2. 1.3

Borg Warner Globe Valve

10 CFR Part 21 Notification

On October

25,

1994,

Borg Warner issued

a

10 CFR Part 21 notification

concerning

a potential

design

problem with 6-inch,

900 psi, motor-operated,

Y-globe valves.

The manufacturer

noted that the stem thrust required to close

the valve should

be based

on the differential pressure

(DP)

on the valve guide

area

instead of the nominal valve seat

area.

This conclusion

was

based

on

testing

conducted

during the Electric Power Research

Institute

(EPRI)

NOV

performance prediction program.

The tests

showed that,

in some cases,

the

required

stem thrust using the valve guide area

was more than double the value

calculated

using the seating

area.

As

a result,

the valves

may not have

enough thrust to close

under actual

DP conditions.

The inspector

asked

the licensee if they were

aware of the

10 CFR Part 21

notification and if they had

any of the susceptible

valves.

The inspector

was

informed that the

HPSI isolation valves,

including Valve SIA-UV-627, were

2-inch,

Borg Warner,

Y-globe valves

and were susceptible

to the problem.

There were eight of these

valves in each of the three units.

The licensee

had

previously determined

during

DP testing that the required thrust to close

these

valves

was higher than the calculated thrust in some cases.

The

licensee

found that in every case

the motor operators

had enough available

thrust to stroke the valves during design basis

DP testing.

The inspector

concluded that there

was not

a safety concern

because

the valves

had

been

successfully

DP tested.

1

The licensee

had previously issued

two condition reports/disposition

requests

(CRDRs) to evaluate

the problems identified during the

EPRI tests

and in the

(

,i

1

10 CFR Part 21 notification.

The licensee

determined that their

HOV 'program

required

a

CRDR to be initiated if the valve factor identified during

DP

testing

was greater

than

85 percent of the

assumed

valve factor.

The

inspector

reviewed the evaluations

and concluded that the licensee's

HOV

program compensated

for the

phenomena

described

in the

10 CFR Part 21

notification.

2.2

Unit

2 Restart

Followin

Hide cle Outa

e

On October

16,

1994, Unit 2 was in the final preparations

for restart

following a midcycle outage to inspect the steam generators.

During the

efforts to restart

the unit,

a number of conduct of operations

problems

resulted

in plant events.

Host significant were

a mai,n feedwater

pump trip

and

a main generator trip, both caused

by operator errors.

These

two events

are discussed

below.

In response

to these

events,

on October

20, operations

management

mandated

changes

to the conduct of operations

which they had planned to implement in

'late-November.

These

changes,

which were developed

through the re-engineering

study,

are discussed

in Section 3.4.

2.2.

1

Hain Feedwater

Pump Trip

On October

17,

1994, with reactor

power at

15 percent

and only one main

feedwater

pump operating,

a reactor operator

(RO) performed

a main feedwater

pump stop valve test,

isolating

steam to the main feedwater

pump.

As

a

result,

level in both steam generators

decreased

rapidly,

and operators

manually initiated auxiliary feedwater

and manually tripped the main turbine

to prevent

a reactor trip on low steam generator level.

The licensee initiated

an investigation of this event.

The licensee

concluded

that the following factors lead to the turbine trip:

~

The

RO performed the stop valve test without using the procedure.

The

procedure

for performing the stop valve test required that the stop valve

test

be performed

when the feedwater

pump turbine is operating

on low

pressure

steam only and the high pressure

control valve is closed.

The

RO did not effectively communicate

his intentions to perform the test

to the rest of the operating

crew or shift management.

~

A test interlock, which should

have prevented

the stop valve from going

closed with the high pressure

control valve open,

was out of adjustment.

The licensee

performed several

corrective actions.

The licensee

removed the

RO involved in the event from licensed duties,

pending operations

management

review of the event.

The licensee

adjusted

and retested

the test interlock

associated

with the high pressure

stop valve.

Additionally, licensee

management

implemented

a set of immediate actions

in order to improve

formality, command

and control,

and performance of the control

room staff

(Section 3.4).,

The inspector

reviewed the licensee's

investigation

and corrective actions

and

concluded that licensee

management

took prompt

and thorough action in response

to the event.'ubsequent

to the implementation of the corrective actions,

the

inspector

noted

an

improvement

in the formality, and

command

and co'ntrol of

the control

room staff.

2.2.2

Generator Trip Due to Auxiliary Operator

(AO) Error

On October

16,

1994,

an

AO misinterpreted

an instruction from the Unit

1

control

room and attempted

to manually close

a motor-operated

disconnect

during the performance of an energy control center switching procedure

and

caused

a main generator trip during the unit startup.

At the time, the main

generator

was turning, but the field was not excited.

The Shift Supervisor

(SS)

had directed

the

AO to verify that the motor operator

mechanism

was

locked in the coupled position

and to remove the energy control center tag.

The licensee

performed

an evaluation to determine if there

was

any damage to

the generator

(which was running at

1800 revolutions per minute

and not

excited),

the motor-operated

disconnect,

and generator

output breakers.

The

licensee

determined

no damage

occurred

and synchronized

the generator

to the

grid several

hours later.

The licensee initiated

an investigation of the event

and identified the

following weaknesses

during the evolution:

~

the

AO did not attend the prejob briefing that was required

by the

sensitive

issues

manual,

~

the

AO did not use

an approved

procedure

to perform the task,

and

, ~

there

was

a communications

breakdown

between

the

AO in the switchyard

and

the Unit 2 control

room.

The inspector

reviewed the licensee's

investigation

and found it to be

thorough.

The inspector will monitor the licensee's

corrective actions

as

part of a future routine inspection.

2.3

Unit 2 Reactor Tri

On October

29,

1994,

the unit sustained

a reactor trip on

a low Departure

from

Nucleate Boiling trip signal

as

a result of an equipment failure when

CEA

Calculator

1 inserted

large penalty factors into the core protection

calculator.

The reactor trip was

an uncomplicated

reactor trip and the unit

was stabilized

in Mode 3.

0'

l

i,

-10-

The licensee

investigated

and repaired

CEA Calculator

1 by replacing the main

processor.

The licensee initiated

a

CRDR to evaluate

the main processor

board

failure.

On October 30, the unit was taken critical and returned to the grid

the following day.

The inspector

responded

to the plant following the unit trip.

The, inspector

determined that the operators

responded

adequately

to the reactor trip.

The

inspector

noted

no deficiencies

in the subsequent

reactor startup

and

power

ascension.

3

OPERATIONAL SAFETY VERIFICATION

(71707)

3. 1

Remote

Shutdown

Panel

Li hts

On October

17,

1994, during routine plant walkdown activities, the inspector

identified that indicating lamps

on the remote

shutdown

panel

(RSP) in Unit 2

were in'correct.

The inspector

observed that several

red, green,

and white

lamp covers,

which indicate equipment status,

had

been

swapped.

The inspector

'notified the

SS of the problem.

The inspector

and

SS inspected

both of the

Unit

2

RSPs

and identified that approximately

20 lamp covers

had

been

swapped,

including changes

between

the two RSPs.

The licensee

subsequently

returned

the panels to their appropriate configuration

and confirmed operability of the

panels.

The licensee

inspected

the

RSPs

in Units

1

and 3,

and other control

and

indication panels

in Unit 2, for proper

lamp covers,

and identified no

additional discrepancies.

The licensee initiated

a

CRDR and

an investigation

to determine

the cause of the event.

The investigation did not reveal

the

person

who swapped

the lamp covers.

The inspector

reviewed the scope of the

licensee's

investigation

and found it to be thorough.

As

a corrective action,

the licensee

issued

a night order to alert all

operations

personnel

to heighten

awareness

concerning

unusual

plant equipment

alignment

and suspicious activities.

The licensee

planned to install locking

mechanisms

on the rear doors to the

RSPs

on all three units,

and modify the

operations

preventative

maintenance

procedures

to include drawings of the RSP.-

In addition,

the licensee

planned to install automatic control

access

devices

(ACAD) readers

at the

RSP

room entrances

in all three units.

The inspector

concluded that operations

performed

a prompt

and thorough

verification of other remote

panel light indications.

The inspector

determined that while the repositioning of the indicating lamps could

initially cause

operator confusion,

the configuration

posed

no significant

problem.'he

inspector concurred with the licensee's

conclusion that the

RSP

was operable

at all times.

3.2

Failure to Meet Commitments

Made in Unit 2 Batter

TS Amendment

On October

13,

1994,

the

NRC granted

an

amendment

to the Unit 2 TS 4.8.2. l.e,

"DC Sources - Operating," to allow Unit 2 to startup

and operate with 125-Vdc

I $

1

-11-

batteries

that did not meet the

TS surveillance

requirement for minimum

battery capacity

(NRC Inspection

Report 50-528/94-31;

50-529/94-31;

50-530/94-31).

In their request for the

TS amendment

dated October

9 and

supplemented

on October

12, the licensee

committed to provided the following

additional controls

and limitations on the maintenance

of important equipment:

~

Probabilistic Risk Assessment

(PRA) would be used to review al'l

125-Vdc

system

and related auxiliaries corrective/preventative

maintenance

work.

~

Access to the switchyard would be limited.

All emergent

switchyard work

would be reviewed

by the Unit

1 SS.

Shortly after the

TS amendment

was issued,

three events

took place which

demonstrated

that the licensee

had not fully implemented

these

commitments.

These

events,

discussed

in detail

below, involved:

~

The construction of scaffolding in two 125-Vdc equipment

rooms for

penetration

seal

work which was not reviewed prior to the start of work.

This was identified by the licensee.

An electrician,

while attempting to reposition

a control

board indication

socket,

caused

a short circuit to ground

on

a 125-Vdc bus.

NRC personnel

found

a switchyard gate

open after -hours

and

had apparently

been left open

by switchyard (nonutility) workers.

3.2. 1

Working in Two Vital 125-Vdc Equipment

Rooms Without

PRA Review

On October

18,

1994,

the licensee initiated the construction of scafFolding in

two Unit 2 125-Vdc equipment

rooms for penetration

seal

work.

On October

25,

the shift technical

advisor noted that the work had not been evaluated

by the

PRA group.

The

PRA group subsequently

reviewed the work and allowed it

to

continue in one equipment

room at

a time.

The licensee

subsequently

initiated

a

CRDR to assess

how this work was missed

and to initiate corrective actions.

The inspector

concluded that the licensee

took prompt action to stop work in

both equipment

rooms

and evaluate

the risk of the work being performed.

The

inspector

noted the alertness

of the

STA to recognize

the problem.

The

inspector

noted that this was

an example of the licensee's

work control

process failing to highlight work requiring

a

PRA review in accordance

with

the

TS Amendment

71,

3.2.2

Working on

a Control

Board Light Socket Without a Work Package

and

Without

PRA Review

On October

26,

1994,

the inspector

observed

arcing in a lamp socket while

performing

a control

board walkdown in Unit 2.

The inspector determined that

t

the arcing

was due to

an electrician attempting to insert the lamp socket

back

into its original position.

The electrician

subsequently

caused

a ground

on

a

e

-12-

vital 125-Vdc bus.

Operations

personnel

directed the electrician to pull the

lamp socket

away from the control

board

and the ground cleared.

The inspector questioned

the electrician

and determined that

he did not have

a

work order

(WO) to perform repairs

on the socket.

The licensee

indicated that

reinserting

1'amp sockets

was

a routine. activity and is often performed without

a

WO.

Based

on the comments,

the licensee

subsequently

issued

a WO'o

complete

the repairs to the

lamp socket

and

a

CRDR to evaluate

the

need for a

WO on this type of activity.

Nevertheless,

since operations

considered

the

lamp socket

work

a routine activity, the, inspector

concluded that the licensee

did not meet the commitments of the October

9 and

12,

1994 letters in that the

licensee

attempted corrective maintenance

on

an indicating lamp socket

powered

by

a 125-Vdc system without prior

PRA review.

3.2.3

Switchyard

Gate Left Open

On October 20,

1994, at approximately

6 p.m.,

NRC personnel

observed that

a

gate leading to the site switchyard

was open.

The gate

was to the main

switchyard, is controlled

by the Salt River Project

(SRP) electric utility,

and is outside the protected

area,

There did not appear

to be anyone working

in the switchyard at the time.

Site security

was notified and the gate

was

secured

at approximately 6:20 p.m.

The inspector notified plant management

of this finding and the licensee

performed

an investigation.

The licensee

contacted

SRP to determine

how the

gate

had

been left open.

SRP technicians

explained that the gate,

which is

not normally used for access

to the switchyard,

was probably opened to provide

a quicker route to the site cafeteria.

The technicians

had not closed the

gate

when they returned

from lunch, or closed it when they left the switchyard

for the day.

The licensee

evaluated this issue in light of their commitment to limit access

to the switchyards.

They determined that action

had

been taken to notify SRP

of the increased

sensitivity to switchyard activities.

However,

SRP

was not

notified formally nor at

a high level.

The licensee

subsequently

performed

followup discussions

with SRP management

to reiterate

the sensitivity towards

switchyard

access

control.

As

a corrective action,

the licensee

was considering establishing

a primary

contact with SRP

and revising switchyard administrative controls procedures

to

ensure that appropriate

communications

are

made in the future when plant

conditions,

such

as the

RCS at midloop, warrant greater

switchyard control.

3.2.4

Conclusion

The inspector considered

these three incidents to be failures of the licensee

to adequately

implement the commitments

made to support the October

13,

1994,

TS amendment

(Deviation 529/9434-02).

l

l'

-13-

3.3

Unit 2 Control

Rods in Hanual

On November 3,

1994,

the inspector

noted that the Unit 2 mode select

switch

(HSS) for the reactor regulating

system

was in manual

sequential

(manual) vice

automatic sequential

(auto).

The inspector questioned

the operators

about the

position of 'the switch and determined that the

HSS was in manual

due to

temperature

oscillations

on the input to the reactor regulating

system

from a

hot leg temperature

instrument.

The inspector

noted that while

a similar

problem exists

on Unit 1, operators

in that unit maintain the

HSS in auto.

The inspector

asked operations

management

to explain the difference.

The licensee

determined that the Unit 2 operators

had placed the

HSS in manual

to address

the possibility of a single failure of the redundant

temperature

input causing

the control

element

assemblies

(CEAs) to automatically respond.

Unit

1 operators

had kept the

HSS in automatic to allow the

CEAs to respond to

a reactor cutback.

Operations

management

determined that the possibility of a

reactor cutback

was more likely than the failure of the temperature

input and

that the

HSS in both units should

be in auto.

The licensee

and Combustion

'ngineering '(CE) were continuing to monitor and evaluate

the hot leg

temperature

anomalies

that

have

been

occur ring on

CE reactors.

The licensee

had initiated

a

CRDR to document

and track the concern

(NRC Inspection

Report

50-528/94-22)

50-529/94-22;

50-530/94-22).

The inspector

agreed with the licensee's

conclusion to place the

HSS in auto.

While the inspector also noted that the licensee

had not addressed

the problem

until questioned

by the inspector,

the licensee

responded

quickly to the

questions.

3.4

0 erations

Standards

On October

19,

1994,

the Executive Vice President

issued

a memo to operations

listing several

revised expectations

for the conduct of operations

and stating

that

he expected

a step

change

in their performance

(NRC Inspection

Reports

50-528/94-34;

50-529/94-34;

50/530/94-34).

On November 7, the director of

operations

held

a day long seminar with the operations

department

leaders

emphasizing

management

expectations

for higher standards

of command

and

control, formality, and professionalism for the operations

department.

The

inspector

found the meeting to be very constructive.

A second

meeting

was

held

on November

18.

The inspector

noted

a general

improvement in control

room operations.

The

inspector

observed that the noise level

and

amount of control

room traffic was

reduced.

In addition,

the control

room communications

between

operations

and

other disciplines

imp'roved.

The inspector

noted that the licensee

intended to

implement the revised operations

standards

in November but implemented

them

earlier due to recent operations

events,

0'

-14-

3.5

S ecial Variance

on Unit 3 Steam Generator

Blowdown Alarm

On October

26,

1994,

the inspector

reviewed the special

variance log in

Unit 3.

Special

variances

are temporary

changes

to procedures

necessitated

by

plant conditions which are anticipated to be temporary.

The inspector

noted

that the log contained

an active special

variance that

was over 8 months old

and

one

on the steam generator

blowdown system alarm response

procedure.

The

licensee initiated the special

variance

on the alarm response

procedure

due to

a degraded

heat

exchanger.

A degraded

heat

exchanger

caused

a high

temperature

alarm in the control

room during certain

blowdown system

alignments

when ambient temperatures

were high.

Subsequent

to initiating this

variance,

the licensee

installed

a temporary modification which injected .cool

water into the ion exchanger

and the system

was

no longer affected

by ambient

temperatures.

The inspector questioned

the onshift crew to determine

whether

the variance to the alarm response

was still required following the

modification.

The

SS concluded that it was not and directed that it be

closed.

The inspector discussed

management's

expectations

concerning

the

use of

special

variances

with the Unit 3 operations

department

leader.

The

operations

department

leader stated that the special

variance

should

be used

when circumstances

required

a deviation from approved

procedures.

The

variation could

be used for a "one time" evolution or be used

numerous

times

until equipment repairs

allow the use of the original procedure.

The

operations

department

leader

expected

the

SS to be familiar with all active

special

variances

and committed to ensure that this was understood

by all

crews.

The inspector

concluded that the use of special

variances

was acceptable.

The

inspector

reviewed licensee

procedures

for special

variance,

for conduct of

operations,

and for shift turnover.

The inspector

noted that none of the

procedures

required

a review of the special

variance log.

Finally, the

inspector

concluded that the two special

variances

in question

had

no safety

impact

on the plant.

3.6

Unit

1

Pressurizer

Vent Valve 0 erabilit

Determination

On November 26,

1994,

the licensee

shut

down Unit

1 to comply with'he

TS

action statement

for an inoperable pressurizer

steam

space

vent path.

The

licensee

had declared

the vent path inoperable

due to the erratic behavior of

the pressurizer

vent Valve RC-103,

and the isolation valve to the reactor

drain tank (RDT), RC-105.

The leakage

from the pressurizer

vent path through

Valves

RC-103

and

105 was first noted in Hay 1994

and

had degraded

significantly since that time.

The inspector

reviewed the licensee's initial

operability determination,

as well as subsequent

evaluations.

In Hay 1994,

the licensee

observed

leakage

from the pressunzer

vent path

through Valves

RC-103

and

RC-105.

The leakage

caused

the pressure

in the

piping between

Valves

RC-103

and

RC-105,

as indicated

on pressure

instrument

(PI)

138, to stabilize at

RCS pressure

of 2250 psi.

The operators

noted that

l

,

t

-15--

after several

days,

the pressure

on PI-138 began to slowly lower until the

closed indication for Valve RC-103 went out.

The closed indication remained

out for about

10 seconds

and

th'en the pressure

on PI-138 increased

and again

stabilized at 2250 psi.

This sequence

occurred

once or twice

a day and then

would not reoccur for up to several

weeks.

The licensee

performed

an

operability determination to consider whether the pressurizer

vent path

was

"closed"

as required

by TS 3.4. 10 when the closed

(green

lamp) indication for

Valve RC-103

was not illuminated.

The licensee

determined that the vent path

was closed

because

redundant

Valve RC-105

had always indicated closed.

The

inspector

reviewed the initial operability determination

and

agreed with the

licensee's

conclusions.

On the morning of November 9, Unit

1 operators

received

several

reactor

coolant vessel

vent/seal

trouble alarms followed by an

RDT high pressure

alarm.

Operators

noted that the pressure

on PI-138 was oscillating between

2250 psi

and

1750 psi every

1 to'

minutes.

During the oscillations,

Valve

RC-103 closed indication would go out and the

open indication would illuminate

for a few seconds

when the indicated pressure

reached

the low end of the band.

The oscillations continued for several

hours until pressure

again stabilized

at 2250 psi.

The licensee

reviewed the original operability determination

and

concluded that the condition observed

on November

9 did not cause

the system

to be inoperable

because

Valve RC-105 always

had indicated shut.

The

inspector

agreed with the licensee's

operability determination.

The inspector

also concluded that the licensee

was sensitive to the changes

in the observed

behavior of the pressurizer

vent system

and the

need to continually assess

the

operability of the system.

On November

24, oscillations

on PI-138

and additional

RDT high pressure

alarms

were noted.

However, rapid pressure

increases

were noted in the

RDT and

on

several

occasions

the closed position indication

on Valve RC-105 was lost,

The licensee

subsequently

questioned

the continued operability of the

pressurizer

vent path since both Valves

RC-103

and

RC-105 lost closed

indication at the

same time.

The licensee

decided to manually isolate the

pressurizer

vent path

and entered

a 72-hour

TS shutdown action statement.

On

November

26, the licensee

shut

down the plant

and entered

Mode

4 to repair

Valves

RC-103

and

RC-105 (Section

4. 1).

The inspector concluded that the

licensee

made

a safe,

conservative

decision to declare

the system inoperable

and shut

down the plant to perform repairs.

4

MAINTENANCE OBSERVATIONS

(62703)

4. 1

Re air of Unit

1 Pressurizer

Head Vent Valves

As noted in Section 3.6 of this report,

on November

26,

1994, Unit

1 shut

down

to repair the pressurizer

head. vent Valve (RC-103)

and the head vent system

drain valve to the

RDT (Valve RC-105).

Both valves

had

been

behaving

erratically.

The inspector

observed

the disassembly

and reassembly

of both valves

and the

subsequent

reinstallation.

The valves. were Target

Rock solenoid-operated

f

I

-16-

valves.

The inspector

observed

that during the reassembly

work, the mechanics

relied heavily on instructions contained

in the vendor technical

manual

(VTH).

However, the

VTH instructions

were not referred to in the maintenance

WO.

.The

WO, which included

some detail

on how to reassemble

the valves,

was

a "model

WO" for the repair of Target

Rock solenoid-operated

valves.

The specific steps

in the

VTH which the mechanics

used involved the'etting of

the stroke

on the pilot valve.

The setup

involved an iterative step in which

tolerances

were measured,

a calculation

was performed to determine if the

stroke

met

an acceptance

criteria,

and, if the acceptance

criteria was not

met, considerable

disassembly,

adjustment,

and reassembly

were performed.

The

inspector

observed that while the mechanics

had

some difficulty initially

doing the iterative step,

they ultimately accomplished

the setup for both

valves.

In

NRC Inspection

Report 50-530/94-26,

the inspector

observed

maintenance

on

an identical valve used

as

a containment isolation valve in the main steam

system

in Unit 3.

The inspector

had identical findings regarding the quality

of the

WO which was derived from the

same

"model

WO".

At that time, the

licensee

had noted that the setup of the pilot valves in Target

Rock valves

was critical to ensure

valve reliability.

In response

to the concern

in

NRC

Inspection

Report 50-530/94-26,

the maintenance

management

initiated

a

CRDR

which included

an action to improve the

"model

WO."

The licensee

had suspected

that the erratic behavior of both Valves

RC-103

and

RC-105 was attributable to degraded pilot valve seats.

This proved to be true

during the disassembly

of the valves.

The inspector

noted that with the

previous

concerns

regarding the quality of the

WO, the importance of the pilot

valve setting,

and the fact that erratic behavior of these

valves

had required

a plant shutdown,

maintenance

had not ensured that the

WOs for Valves

RC-103

and

RC-105

had

been modified.

The inspector

planned to perform

a followup inspection to determine

why

problems continue to exist in the

WO.

This is

an Unresolved

Item (Unresolved

Item 528/9434-03).

4.2

Other Haintenance Activities Observed

The inspector

observed

portions of the maintenance activities noted

below.

The activities observed

were performed appropriately.

~

Unit

1 pressurizer

spray valve maintenance,

~

Unit

1 removal of spent fuel pool blocking plates,

and

~

Unit 2 fire penetration

seal repairs.

-17-

5

EMERGENCY PREPAREDNESS

DRILL (71750)

On November

16,

1994,

the inspector

observed

the licensee

performance

during

an emergency

plan drill.

The drill involved activation of the emergency

operations facility (EOF)

and limited State

and local participation.

The

drill scenario

involved

a steam generator

tube rupture,

main steam line break,

and

some fuel failure, resulting in an offsite release.

The resident

inspector

responded

to the simulator

and the senior resident

responded

to the technical

support center

(TSC).

The resident

inspector noted

the operations

advisor did

a good job maintaining the professionalism of the

operations

crew.

The inspector noted adequate

communications

between

the

operations

personnel

and

between

the simulator

and the TSC.

The senior resident

observed

good communications

between

the

TSC staff,

and

the simulator

and

EOF.

The inspector

noted that this was the most extensive

drill in which the emergency

response facility data acquisition display system

was used.

The computer

system,

which provided real time plant data to the

TSC

and

EOF,

appeared

to provide

a substantial

amount of information, easing

the

event diagnosis

and response.

6

ONSITE ENGINEERING (37551)

6. 1

S ent fuel Assembl

Reshuffle

A TS amendment

was recently approved to change

the storage

mode of the spent

fuel pool from a checkerboard

mode

(two out of every four locations with spent

fuel) to

a high density

mode.

The revised

TS a'llowed the spent fuel pool to

be divided into three regions.

Region I of the spent fuel pool remained

a

checkerboard

pattern,

region

2 would be

a three out of four pattern,

and

region

3 would be

a four out of four storage pattern.

The fuel assemblies

were stored

in the region

based

on fuel burnup, with the highest

burnup

assemblies

stored

in the four out of four region.

On November 9, the inspector

reviewed the

WO and observed

portions of the

reconfiguring of the spent fuel pool in Unit 1.

The inspector

noted

good

radiological

and foreign material controls

by the personnel

involved in the

evolution.

The inspector concluded that engineering

had established

appropriate

controls

to determine

the proper location of the fuel assemblies.

Additionally, the

inspector

noted that

a

100 percent verification of the proper configuration of

the spent fuel pool

was conducted after the movement of all the spent. fuel

assemblies,

0

-18-

7

EVALUATION OF ONLINE NAINTENANCE (TI 2515/126)

The inspector

reviewed the licensee's

process for scheduling online

maintenance.

The inspector

reviewed the licensee's

procedures,

interviewed

individuals from site scheduling,

the

PRA

group probable risk assessment,

and

operations.

The purpose of this inspection

was to review maintenance

scheduling activities with respect

to risk management

in accordance'ith

NRC

Inspection

Manual TI 2515/126.

7. 1

Schedulin

Process

Develo ment

The inspector

reviewed the scheduling

and planning processes

for online

maintenance

with members of the site scheduling organization.

The licensee

uses

a 12-week scheduling matrix for planning maintenance.

The licensee

chose

a 12-week vices

a 13-week schedule

so that maintenance

and testing activities

could

be performed

on the

same

day of the week while meeting monthly frequency

requirements.

The matrix coordinates

the scheduling of planned

maintenance,

and surveillance testing

by the week.

The licensee

developed

the matrix

'starting with surveillance testing requirements.

Systems that required

attendant

equipment to be operable

were grouped together.

The licensee

spaced

the testing

so that redundant train components

were not tested

during the

same

week.

The licensee

used

these

scheduled

test

windows to coincide with planned

outage

availabilities.

This way, the licensee

was able to use

a scheduled

routine

surveillance test to demonstrate

system operability following maintenance.

Finally, the licensee

reviewed all preventative

maintenance activities.

The

most frequent activity was

used to develop the online maintenance

window.

For

example,

each

emergency

diesel

generator

(fDG) is tested

on

a monthly basis

and the most frequent preventative

maintenance

is required every

6 months.

Therefore,

the licensee

has

an online maintenance

window every

6 months or

every other

12 week schedule.

Additionally, maintenance

required

on the spray

pond or other systems

required for fDG operability are scheduled

concurrently

with the

fDG.

7.2

Schedulin

Process

Risk Assessment

0

The

PRA group reviewed the scheduling matrix to ensure that the scheduled

activities did not introduce unacceptable

risks to the plant.

The

PRA group

reviewed the matrix for unacceptable

risk combinations.

This included

a

review to ensure that divergent

systems

necessary

for accident mitigation were

not scheduled

concurrently.

For example,

the matrix schedules

activities

on

the high pressure

SI, low pressure

SI,

and containment

spray

pumps

on separate

weeks since they all may be required for similar accident mitigation purposes.

7.3

~Schedulin

Using the

12-week scheduling matrix, the licensee lists routine work requests,

preventative

maintenance,

and

WOs to the assigned

outage

window.

Four weeks

prior to the work week,

the licensee

performs

an item-by-item review.

Two

i

-19-

weeks prior to the work week,

the licensee

conducts

another

review and

develops

a final approved

work list.

Finally, site scheduling

conducts daily

meetings with operations

and maintenance

to review the items scheduled

for the

next

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

I

The impact'f emergent

work activities

on core

damage

frequency ultimately is

the responsibility of the operating

crew.

The licensee

procedure for hanging

a clearance

requires

the operating

crew check that redundant trains of

equipment

are available prior to hanging the clearance.

Additionally, if one

train of equipment is already out of service for maintenance

when

a component

fails, the operating

crew is responsible

to initiate the required

TS action

statement.

Finally, the inspector

has

observed

that the operating

crews

inform their management

of all priority one

and

two work requests

to ensure

that management

is involved in the decision

making process.

Priority one

and

two work requests

are those that require

immediate action to protect

individuals and/or equipment

and those that must

be worked within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />

due

to

a TS.

The

PRA group was involved in the scheduling

process

mainly in the development

and approval of the

12-week scheduling matrix.

However, if unusual

circumstances

occur, site scheduling

may request

that the

PRA group review the

weekly schedule.

For example,

Unit 2 has

a degraded

condition on all four

class

1E batteries

and

has committed to the

NRC to minimize activities

affecting the class electrical

system

(Section 3.2).

The

PRA group reviews

and approves

the scheduled

work activities which may impact the electrical

system.

The inspector

concluded that this approach

required site scheduling

to identify unusual

circumstances

and

had the potential to overlook less

obvious interactions.

7.4

Future Schedulin

Develo ments

0

The licensee

was in the process

of implementing

an integrated

scheduling

matrix that coordinated

the testing

and maintenance activities of all three

units.

This was

a result from the recently reengineered

maintenance

organization

where the licensee

combined three

separate

organizations

into

one.

The licensee

anticipates

two benefits to the integrated

schedule.

First, it should reduce

the manpower

burden

on the maintenance

organization

by

ensuring

maintenance

activities are not scheduled

on the

same

system in more

than

one unit.

And second, it should

reduce

the probability that the

same

type of human error-caused

failure could

be introduced in more than

one unit.

Finally, the licensee

was in the process of developing

a visually oriented

matrix for determining the risk associated

with different combinations of

system unavailabilities.

The licensee

performed

a detailed

PRA review of

potential

combinations

and categorized

each

one according to the associated

increase

in core

damage

frequency

(CDF).

The licensee

used the

EPRI

guidelines

to develop the following coding

scheme:

green or acceptable

activities increase

the

CDF by less

than

10E-6, yellow or caution activities

increase

the

CDF by between

10E-6

and

10E-5,

and red or dangerous

activities

increase

the

CDF by more than

10E-5.

The matrix also

shows which combinations

If

1

fi

I

1

0

-20-

would place the unit in

a

TS 3.0.3 action statement

and require

immediate

action to restore

systems

or shut

down the unit.

The licensee

intended to

implement this matrix by February

1995.

The inspector

reviewed

a draft of

this matrix and found it to be easy to understand

and apply to plant

configurations.

7,5

Conclusions

The inspector

concluded that the licensee

had

a process for scheduling online

maintenance

that appropriately

considered risk aspects

of those activities.

The licensee's

program involved the

use of a simple matrix system that

had

been thoroughly reviewed

by the risk assessment

group.

The inspector

concluded that the licensee

reduced

system

outage

times

by performing online

maintenance

on systems

concurrent with their required preventative

maintenance

and with maintenance

on their attendant

systems,

The inspector

noted that the

PRA group was not involved in maintenance

scheduling

on

a daily basis

unless

requested

and that this had the potential for missing risk significant

'ombinations.

However,

the inspector

concluded that the licensee's

planned

implementation of a visually-oriented risk matrix would lessen this potential.

8

PLANT SUPPORT

(71750)

8.1

Securit

Findin

s

On November

15,

1994,

the inspector

observed

a contract

employee

not wearing

an

ACAD inside the protected

area.

The inspector notified security,

who

subsequently

took custody of the person.

The inspector

noted that the contract

employee failed to properly wear the

ACAD, failed to notify security of the misplaced

ACAD, and did not

know of the

requirement

to notify security

when misplacing

an

ACAD,

The inspector determined that security performed adequately

when informed

about the lost ACAD,

Security determined that the worker had left the

ACAD in

a locker.

Although the worker had received

access

training

4 months prior to

this protected

area entry, this had

been the worker's first entry into the

protected

area.

The inspector

noted that the licensee

counseled

the

individual about

ACAD control.

The inspector

determined

the safety

significance of the event

was low.

8.2

Protected

Area Access Turnstile

After entering the protected

area,

the inspector

noted that the turnstile

continued to rotate

beyond the 120'F rotation necessary

for protected

area

access.

The inspector

continued to rotate the turnstile until it latched

after rotating approximately

240~F.

The inspector notified security

concerning

the turnstile.

The turnstiles

are full height access

devices that

allow one person to enter for every 120'F of rotation.

,jl

-21-

A security sergeant

explained that the turnstile latch was designed

to be

free'ong

enough for one person to enter

and then relatch

when the turnstile

reached 120'f rotation.

The sergeant

demonstrated

that if the latch

becomes

worn and the turnstile were rotated quickly enough,

that it can

be rotated

beyond 120'here it will not be aligned

and cannot latch.

However, if the

turnstile were left in this position for a few seconds, it would latch after

an additional 60'f rotation.

The inspector

noted that if an unauthorized

individual attempted

entry in this case,

the individual would be locked

between

the security bars.

Security tested

the turnstile several

times

and noted that while it usually

did latch after 120', it did on occasion

continue to 240'.

Security promptly

locked the turnstile in position

and initiated

a work request.

The inspector

concluded that the licensee

took appropriate

action.

9

FOLLOWUP OPERATIONS (92901)

9. 1

0 erabilit

Determination

Procedure

Im lementation

During

a routine tour of the plant the inspector

noted that the automatic

makeup valve for the essential

cooling,water expansion

tank was isolated.

The

inspector

noted that the automatic

makeup function was described

in the

Updated Final Safety Analysis Report

(UFSAR)

and that the valve was isolated

because it failed to stop flow.

The inspector discussed

the existing

condition with the system engineer

and noted that

a

WO and

a

CRDR had

been

written documenting

the condition

and that

a

10 CFR 50.59 safety evaluation

was performed to address

the fact that the automatic

makeup function was

disabled,

the inspector

concluded that the manual

actions

were acceptable

substitutes.

The inspector

conducted

a review of the licensee's

operability determination

procedure

and noted that

a new appendix

was

added that outlined the required

reviews

when

a manual

action

was substituted for an automatic function.

The

inspector

reviewed the operability determination

log and- noted that the

actions outlined in Appendix

C of the operability determination

procedure

were

not performed for the essential

water surge tank automatic

makeup valve,

't

The inspector

asked

the licensee

why an operability determination

was not

performed.

The licensee

determined that Appendix

C was not part of the

procedure

when the condition was identified in Hay 1994.

At that time,

an

o'perability determination

was not required since existing documentation

in the

form of the

CRDR and

10 CFR 50.59 safety evaluation

already existed.

Appendix

C was

added to the operability determination

procedure

in July 1994.

However,

the body of the procedure

was not updated to describe

the purpose of

Appendix C,

and

when the actions

were required.

The inspector discussed

the apparent

oversight in the operability

determination

procedure with operations

management.

The inspector

reviewed

the manual

actions for essential

water surge tank makeup

and found them to be

consistent

with the manual

action criteria discussed

in Appendix

C of the

J'

'I

'f

i

'fir

-22-

licensee's

operability procedure.

The licensee

agreed to review the procedure

to determine if any improvements

were needed.

The licensee

also

agreed

to

review all the automatic functions that were bypassed

by manual

actions to

ensure that the intent of the Appendix

C actions

were being met.

The

inspector

concluded that management's

response

to this concern

was prudent.

9.2

Violation 528 9422-01

Closed

and

LER 528 94-05 Revision

1

Closed

Failure to Ad ust Core Protection Calculator

CPC

Delta-T Power

This violation involved the failure to declare

channel

"D" CPC inoperable

when

a

TS calibration check could not be adequately

performed

due to large swings

in calculated

thermal

power.

The licensee

determined that the root cause of the violation was

a failure of

management

to aggressively

pursue all aspects

of a known problem with

fluctuations in hot leg temperature

(T).

Although engineering

had identified

the root cause of the

T fluctuations,

management

did not pursue whether

operators

could conduct

a reasonable

channel calibration check between

thermal

power and secondary calorimetric power with the existing fluctuations in T.

The licensee

conducted

a review of the four channels of CPCs in all three

units to determine

whether they were operable with the

T fluctuations.

They

determined that calculated

thermal

power fluctuated

about 4-7 percent

on all

12 CPCs.

The licensee

conducted

an evaluation

which determined that the

fluctuations in thermal

power were caused

by the

known fluctuations in T.

Additionally, engineering

determined that the calculated

mean of the recorded

thermal

power was within H percent of the actual

power and that the values

recorded

by the operators

during tests

were very close to the mathematical

mean of the thermal

power.

Based

on this review, the licensee

determined that

all the

CPCs were operable.

The inspector

agreed with the licensee's

conclusion.

The operators

had

been performing

an average of the

CPC digital display of

thermal

power

and recording that value during the channel calibration check.

The licensee

issued

a new procedure,

"Dampening/Averaging of Instrument

Fluctuations," to provide operators

with formal guidance

on

how to record

a

specific parameter, when the corresponding

instrument oscillates

excessively.

The procedure directs the operators

to record the displayed

thermal

power

every minute for a total of 10 minutest

These

values

are then

averaged

and

compared to the secondary calorimetric power to see if a channel

calibration

is required.

The inspector

noted that this procedure

should

he] p ensure

consistency

in the performance of the channel calibration check.

The licensee

used

a new analytical

model to verify that the fluctuations in T

were being caused

by the

known phenomena

of hot leg stratification.

During

this review, engineering

noted that

some utilities either average

the value of

T before

sending

the signal to the

CPC or have all the

T temperature

detectors

in the upper portion of the hot leg.

The licensee

was evaluating

moving the two lower T temperature

detectors

into the two spare wells in the

0-

-23-

upper part of the hot leg to minimize the fluctuations in T>.

The inspector

concluded that engineering

had conducted

a thorough review of the issue.

9.3

Closed

Violation 530 9420-01:

Im ro er Startin

of Steam-Driven

Auxiliar

Feedwater

AFW

Pum

This violation involved Unit 3 operators

that did not follow the procedure

when they attempted

to start the steam-driven

AFW pump with a cold steam

supply line.

As

a result,

condensation

formed when the supply steam contacted

the'0'F

steam piping and caused

the

pump to trip on mechanical

overspeed.

The licensee

determined that poor communication

between

the

RO and control

room supervisor

caused this event.

The licensee

recently

implemented

new

communications

and conduct of operations

standards

to minimize communication

errors.

The inspector

noted that communications

standards

had previously

existed,

but were not being consistently

used during routine evolutions.

The

inspector

noted that management

was emphasizing their expectations

for proper

communications

during all levels of control

room activities (Section 3).

The

inspector recently observed

good closed

loop communication during various

types of control

room evolutions indicating that these

expectations

were being

implemented.

The licensee

also determined that

a procedural

weakness

contributed to the

error.

Specifically, the surveillance test procedure

did not include

steam

line temperature limits in the precautions

and limitations section of the

procedure.

The licensee

updated

the surveillance test to clearly describe

the

steam line temperature

requirements.

An appendix of the procedure

was also

created

to describe

the locations for taking the temperature

of the steam

line.

The inspector

reviewed the procedures

and concluded that the procedure

clearly described

the precautions

and contingencies for low steam line

temperatures.

10

FOLLOWUP - MAINTENANCE (92902)

10. 1

Closed

Followu

Item 528 9355-02:

Pressurizer

S ra

Valve

Maintenance

This open item involved the failure to incorporate

engineering

information

concerning

a revised

bench set into a

WO to calibrate the pressurizer

spray

valve.

The licensee

had previously determined that the bench set information

in engineering

evaluation

requests

(EERs) from 1987

and

1988 had not been

updated

in the equipment

information data

base.

As

a result,

the appropriate

bench set

was not included in the

WO instructions.

The licensee

wrote

a

CROR in response

to the inspector's

concerns

to evaluate

the root cause of the problem

and to determine if there were

any programmatic

weaknesses

that contributed to the error.

The licensee

determined that the

EER procedure

was revised

in 1991 to require

a

CRDR to document

and track any

corrective actions resulting

from EERs.

Prior to 1991, actions resulting from

nonsafety-related

EERs were not formally documented

and tracked,

In the case

of the pressurizer

spray valve,

a

WO was written to update

the nameplate

data

but, was later canceled.

In 1991,

the licensee

conducted

a review of 20 percent of all the closed

design

change

EERs

and determined that only two out of 33 followup actions

were not tracked.

The licensee

canceled

the

EER program in September

1994

and

all engineering

information has since

been

processed

using the

CRDR program.

The licensee

concluded that based

on the previous review of EERs,

an

additional

review of all

EERs prior to 1991

was not required.

The licensee

also concluded that the current process

was adequate

to trend, track,

and

transfer design information, lessons

learned,

and followup actions into plant

maintenance

and practice.

The inspector

reviewed the licensee's

evaluation

and

agreed with the licensee's

conclusions.

11

FOLLOWUP ENGINEERING/TECHNICAL SUPPORT

(92903)

11. 1

Followu

Item 529 9402-02

Closed

HPSI

Pum

Seal

Leaka

e - Unit 2

'This item involved the

HPSI

pump seal

leakage limits.

The inspector

had noted

that the

UFSAR had stated that the

maximum allowed seal

leakage

was

100 cc/hr

and that the licensee

did not have

a surveillance test which limited the seal

leakage

to this value.

The inspector

had noted that the licensee's

surveillance test for the emergency

core cooling system

(ECCS) limited the

entire

system to less

than

1 gallon per minute,

but that there

were

no

specific limits for pump seal

leakage.

The inspector

had questioned

the

licensee

on the basis for the limit and whether the licensee

adequately

measured

this limit.

The inspector

reviewed the licensee's

response

to this issue.

The licensee

stated that the

100 cc/hr seal

leakage limit was

a design input assumption

used for calculating

dose

and

was

an input to the radioactive

waste drainage

system.

The

UFSAR states

that the radioactive

waste drainage

system

was

designed

to handle

up to 50 gallons per minute

and could easily handle the

ECCS leakage of

1 gallon per minute.

The licensee

had contacted

CE for the

basis for the limits.

CE stated that the limit was simply used for design

input used during evaluation for habitability and dose calculations.

During the review of the questions

raised

by the followup item, the licensee

identified that its dose

assessment,

Calculation

13-NC-ZY-209,

assumed

1500

cc/hr leakage

from the

ECCS,

however,

the licensee's

TS Surveillance

requirements

limited the total

ECCS leakage

at

1 gallon per minute.

The

licensee

reviewed the

UFSAR dose

assessment

and determined that it included

enough margin to increase

the

ECCS leakage

from 1500 cc/hr to

1 gallon per

minute

and not exceed

the

10 CFR Part 100 limits for offsite dose.

The

.

inspector estimated

the increase

in offsite dose

was caused

by raising the

ECCS allowable leakage

from 1500 cc/hr to

1 gal/min

and concurred that the

dose did not exceed

Part

100 limits.

The licensee

reviewed the past

15 performances

of the

ECCS leakage testing

and

noted that the total

leakage

was greater

than

1500 cc/hr on five occasions,

l

i

-25-

but always

remained

below

1 gallon per minute.

The licensee

conservatively

decided to revise the surveillance test

acceptance

criteria to z 1500 cc/hr

for the

ECCS.

The inspector

reviewed the surveillance test procedures

for

each unit and confirmed that the acceptance

criteria had

been revised to

~ 1500 cc/hr.

The inspector

concluded that the licensee

met

10 CFR Part 100

limits and the surveillance test adequately

measured

the

ECCS leakage.

11.2

Followu

Item 528 9348-04

CLOSED

MSSV Testin

0

This open item involved an evaluation of the apparent differences

between

MSSV

setpoint testing using the Furmanite "Trevitest" and the Westinghouse

live

steam test

methods

to determine if these differences

could affect the

operability of MSSVs.

The licensee

determined

there

was

an apparent offset

between

the two methods

during

MSSV testing in September

1993.

In March

1994,

Furmanite

informed the

NRC that the valve disk seat

area for the Dresser

Model

3707R safety valve used

in the equation to calculate

the lift setpoint

should

be changed

to match the actual

setpoint during full pressure lift

tests.

This change

was

based

on comparison testing

conducted

at the

Westinghouse test facility between

the two approved test methods.

On August 11,

1994,

the

NRC issued

IN 94-56,

"Inaccuracy of Safety Valve Set

Pressure

Determinations

Using Assist Devices."

The

IN described

how the

change

in valve disc area

would cause

the calculated lift setpoint to be about

one percent

lower.

In response

to the IN, several utilities had to declare

MSSVs inoperable

because

the revised lift setpoint

using the

new seat

area

was

outside

the

band required

by the plant TS.

Operability of the

MSSVs at Palo

Verde was not affected

because

the licensee

had already factored in the offset

into their equation for determining the lift setpoint.

Additionally, the

licensee

had

used

the live steam tests

at the Westinghouse facility to

establish operability of the

MSSVs.

The inspector

noted that the licensee

had

aggressively

pursued

the resol,ution of these testing differences.

12

ON-SITE REVIEW OF LERs

12, 1

LER 529 91-005

CLOSED

HSSV Set oint Out-of-Tolerance

This

LER involved

a significant number of MSSVs having setpoints

during

testing outside the al percent

band required

by the plant TS.

On Hay 16,

1994,

the

NRC issued

a

TS amendment

to increase

the

MSSV setpoint tolerance

from +I percent to a3 percent.

This

LER is closed

based

on the change

in

allowable setpoint tolerance.

13

IN-.OFFICE REVIEW OF LERs

(90712)

The following LERs were closed

based

on

an in-office review:

~

LER 529/94-02:

Reactor Trip and Containment

Spray

~

LER 530/94-05:

Reactor Trip Caused

by Degradation of Feedwater

Flow

Q,y

l

,~

I

~

-26-

LER 530/94-06:

Shutdown Cooling Loop Inoperable

Due to

Pump Breaker

Racked in the Test Position

LER 530/94-07:

Reactor Trip Caused

by an Increase

in Hain Feedwater

Flow

I

4

ATTACHMENT 1

1

Persons

Contacted

1. 1

Arizona Public Service

Com an

J.

  • D
  • W.
  • A.
  • D
  • J
  • D
  • W.
  • 'G

F,

    • G

D.

  • R.

J,

Bailey, Vice President,

Nuclear Engineering

and Projects

Garchow, Director, Engineering

Grabo,

Section

Leader Compliance,

Nuclear Regulatory Affairs

Ide, Director, Operations

Krainik, Department

Leader,

Nuclear Regulatory Affairs

Larkin, Senior Engineer,

Nuclear Regulatory Affairs

Levine, Vice President,

Nuclear Production

Mauldin, Director, Site Maintenance

and Modifications

Montefour, Senior Representative,

Management

Services

Overbeck, Assistant to the Vice President

Nuclear Production

Riedel,

Department

Leader,

Unit 2 Operations

Seaman,

Director, Nuclear Assurance

Shanker,

Department

Leader,

Nuclear Assurance

Engineering

Smith,

Department

Leader,

Unit

1 Operations

Stroud,

Consultant,

Nuclear Regulatory Affairs

Taylor, Department

Leader,

Unit 3 Operations

1.2

NRC Personnel

  • K. Johnston,

Senior Resident

Inspector

H. Freeman,

Resident

Inspector

  • J.

Kramer, Resident

Inspector

  • A. MacDougall,

Resident

Inspector

1.3

Others

  • J.

Draper, Site Representative,

Southern California Edison

  • R. Henry, Site Representative,

Salt River Project

  • F.

Gowers, Site Representative,

El

Paso Electric

  • denotes

personnel

listed above

who attended

the Exit meeting held on

November 30,

1994.

2

EXIT MEETING

An exit meeting

was conducted

on November 30,

1994.

During this meeting,

the

inspector

summarized

the scope

and findings of the report.

The licensee

acknowledged

the inspection findings documented

in this report.

The licensee

did not identify as proprietary

any information provided to, or reviewed by,

the inspectors.

i

I

I

ATTACHMENT 2

ACRONYMS

ACAD

AO

ARP

CDF

CE

CEA

CPC

CRDR

DP

ECC

ECCS

EDG

EER

EOF

EPRI

HPSI

IN

IV

LER

MOV

MSS

MSSV

PI

PRA

RDT

RCS

RO

RRC

RSP

SI

SIT

SRP

SS

TH

TS

TSC

UFSAR

VTM

WO

automatic control

access

device

auxiliary operator

annunciator

response

procedure

core

damage

frequency

Combustion

Engineering

control element

assembly

core protection calculator

Condition Report/Disposition

Request

differential pressure

energy control center

emergency

core cooling system

emergency 'diesel

generator

engineering

evaluation

request

emergency

operations facility

Electric Power Research

Institute

high pressure

safety injection

Information Notice

independent verification

Licensee

Event Report

motor operated

valve

mode select

switch

main steam safety valves

pressure

instrument

probabilistic risk assessment

reactor drain tank

reactor coolant system

reactor operator

reactor regulating

system

remote

shutdown

panel

safety injection

safety injection tank

Salt. River Project

Shift Supervisor

hot leg temperature

Technical Specifications

technical

support center

Updated

Final Safety Analysis Report

vendor technical

manual

work order

1

i'

I

l

~