ML17312B745

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Insp Repts 50-528/97-16,50-529/97-16 & 50-530/97-16 on 970907-1018.Violation Noted.Major Areas Inspected:Operation, Maint,Engineering & Plant Support
ML17312B745
Person / Time
Site: Palo Verde  Arizona Public Service icon.png
Issue date: 10/29/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML17312B743 List:
References
50-528-97-16, 50-529-97-16, NUDOCS 9711060133
Download: ML17312B745 (36)


See also: IR 05000528/1997016

Text

ENCLOSURE 2

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket Nos.:

License Nos.:

Report No.:

Licensee:

Facility:

Location:

Dates:

Inspectors:

Approved By:

50-528

50-529

50-530

NPF-41

NPF-51

NPF-74

50-528/97-1 6

50-529/97-1 6

50-530/97-1 6

Arizona Public Service Company

Palo Verde Nuclear Generating Station, Units 1, 2, and 3

5951 S. Wintersburg Road

Tonopah, Arizona

September

7 through October 18, 1997

Jim Moorman, Senior Resident Inspector

Nancy Salgado,

Resident Inspector

Dan Carter, Resident Inspector

John Kramer, Resi'dent Inspector, San Onofre Nuclear Generating

Station

Dennis F. Kirsch, Chief, Reactor Projects Branch F

Attachment:

Supplemental

Information

97ii060i33 97i029

PDR

ADQCK 05000528

6

PDR

-2-

EXECUTIVE SUMMARY

Palo Verde Nuclear Generating Station, Units 1, 2, and 3

NRC Ihspection Report 50-528/97-16; 50-529/97-16; 50-530/97-16

~Oerations

On September 8, 1997, the Unit 2 reactor coolant system was drained to the hot

midloop condition by a dedicated midloop operating crew which augmented

the

normal operating crew during the evolution.

Operator oversight and direction of the

evolution and decisions to take conservative actions during the evolution were

excellent.

The use of a designated

midloop operating crew was seen as a strength

(Section 01.1) ..

On October 6, 1997, the Unit 2 reactor coolant system was drained to the cold

midloop condition.

A dedicated

midloop operating crew augmented

the normal

operating crew during the evolution.

During the draindown,

a discrepancy between

the "A" and "B" channels of reactor water level indication system was discovered,

which was caused by an open shutdown cooling bypass-valve.

This resulted in less

than 3780 gpm of flow through the core, a violation of TS 3/4.4.1.4.2.

Operator

oversight and direction of the evolution and decisions to take conservative actions

related to the discrepancy observed with reactor level measurement

were excellent.

Immediate corrective actions were timely (Section 01.4).

Observation of core offload and reload activities associated

with the Unit 2,

Cycle 7, refueling outage indicated that refueling personnel consistently used good

communications

and demonstrated

a safety-conscience

approach to performing

refueling operations.

Personnel

performance was excellent (Section 01.2).

In response

to the unexpected

loss of power to the PBB-SO4 4160V Class

1E Bus

on September

17, 1997, the control room operations staff responded

in an excellent

manner (Section 01.3).

Maintenance

Maintenance

and surveillance activities observed

by the inspectors were generally

conducted

in a'safety conscious

manner by knowledgeable

technicians using

current procedures

(Section M1.3).

The inspectors verified that the licensee conducted the Unit 2 containment close out

activities in a thorough manner (Section M2.1).

The licensee installed steam generator

(SG) nozzle dams in the Unit 2 SG during the

Cycle 7 refueling outage to support eddy current testing of the SG tubes.

The

licensee did not provide the foreign material exclusion (FME) responsible

person the

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viewing point and communication tools to properly monitor all items entering. and

exiting the SG Zone III area; a weakness that has since been corrected.

However,

the licensee's

SG nozzle dam installation procedure

and FME training provided to

the nozzle dam installers ensured that acceptable

FME practices were maintained

(Section M3.1).

\\

~

When calibrating the refueling water level indication system detectors to support the

Unit 2, Cycle 7, refueling outage, Instrumentation 5 Controls (l8cC) personnel failed

to adhere to procedural guidance.

This resulted in a non-conservative

eight inch

error in reactor water level indication.

The noncited violation of procedures

represents

poor work practices by the technicians.

The licensee's corrective

actions were sufficiently complete and thorough (Section M4.1).

~En ineerin

~

The engineering department performed an accurate calculation and generated

a

good temporary procedure to verify the adequacy of the shutdown cooling system

to cool the fuel in the reactor vessel and supplement the spent fuel pool cooling

system, as required in the Updated Final Safety Analysis Report (UFSAR). Although

calculations indicated performance of this test was unnecessary,

the licensee's

decision to verify the calculations through performance of the test was a good

example of conservative plant operations

(Section E1.1).

Plant Su

ort

~

.

The licensee removed the Unit 2 core barrel during the Cycle 7 refueling outage for

the 10 year inservice inspection.

The licensee's thorough planning, coordination of

activities, and training of personnel resulted in a'successful

removal of the core

support barrel from the reactor vessel with minimal radiation exposure to personnel.

The licensee's activities to ensure that radiation dose rates remained low were

, excellent (Section R4.1).

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Re ort Details

Summar

of Plant Status

Units

1 operated at essentially 100 percent power for the duration of the inspection period.

Unit 2 began this inspection period in Mode 6. The unit was in midloop operation on two

occasions,

once on Se'ptember 8-9, 1997, (Section 01.1) and the second time on

.

October 6, 1997 (Section 01.4).

On October 11, 1997, the unit commenced

a reactor

startup and power ascension.

The unit reached

100 percent power on October 17, 1997,

and remained there for the duration of the inspection period.

Units 3 operated at essentially 100 percent power until October 7, 1997, when the unit

was reduced to 87 percent power for approximately 7.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> to replace

a failed pressure

switch in the steam plant.

The unit was returned to 100 percent power and remained at

that power level for the duration of the inspection period.

I. 0 erations

01

Conduct of Operations

01.1

Unit 2 Midloo

Reduced

Inventor

Activities

a.

Ins ection Sco

e 71707

On September

8, 1997, the inspectors observed control room operators draining the

reactor coolant system

(RCS) using Procedure 40OP-9ZZ16, "RCS Drain

Operations," Revision 8. The unit was being placed in midloop conditions to install

SG nozzle dams in preparations for eddy current testing.

The inspectors reviewed

the preoutage

midloop training video, RCS draining procedures,

and attended the

briefing before the draining operation.

b.

Observations

and Findin s

The inspectors attended the briefing for the midloop evolution.

The midloop control

room supervisor conducted the briefing professionally with the appropriate nuclear

safety focus.

The inspectors

also reviewed the licensee's

Procedure 400P-9ZZ16,

prior to the reduction of RCS inventory and verified that the prerequisites

were met.

The licensee augmented

the onshift operating crew with a dedicated

midloop team

to perform the midloop operation.

The midloop team was comprised of a control

room supervisor,

a reactor operator, and shift technical advisor who was acting as

midloop coordinator.

The inspectors observed that the midloop team

maintained

positive control of the evolution.

The licensee minimized unnecessary

work while the unit was in a reduced inventory

condition.

To prevent loss of shutdown cooling or RCS level perturbations,

the

licensee incorporated

a supplemental

senior reactor operator (SRO) who was

stationed at the entry of the auxiliary building to screen work activities going into

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the field.

In addition, the licensee maintained sources of offsite and onsite power

available, and limited access to critical equipment areas.

During the draindown, at approximately the 103 foot 8 inch level, the midloop crew

identified that refueling water level indication system (RWLIS) instrumentation was

remaining constant.

At this point, level should have been indicating a continued

reduction.

The operators stopped the draindown and determined that a calibration

problem existed with both channels of the RWLIS. The miscalibration of the RWLIS

is discussed

further in Section M4.1,

Unit 2 was in midloop operation for approximately 14 hours1.62037e-4 days <br />0.00389 hours <br />2.314815e-5 weeks <br />5.327e-6 months <br />.

During that time the

licensee implemented and maintained the requirements

specified by

Procedure

400P-9ZZ1 6.

C.

Conclusion

On September

8, 1997, Unit 2 was drained to the hot midloop condition by a

dedicated midloop operating crew which augmented

the normal operating crew

during the evolution.

Operator oversight and direction of the evolution and

decisions to take conservative

actions during the evolution were excellent.

The use

of a designated

midloop operating crew was seen as a strength.

01.2

Full Core Offload and Reload

Unit 2

aO

Ins ection Sco

e 60710)

The inspectors reviewed, in part, the licensee's performance of a full core offload

and reload as controlled by Procedure 72IC-9RX03, "Core Reloading," Revision 9.

b.

Observations

and Findin s

Unit 2 refueling operations were observed during the period.

The refueling SRO was

in charge of the overall fuel movement process,

and was stationed

in containment

to directly supervise

core alterations.

AIIfuel movement was coordinated with the

control room and logged in accordance with Procedure 72IC-9RX03.

Good

communications were observed between the refueling SRO, the fuel pool bridge

operator, and the control room.

The inspector independently verified that both

startup channels were operable during the fuel movement.

C.

Conclusions

Observation of core offload and reload activities associated

with the Unit 2,

Cycle 7, refueling outage indicated that refueling personnel consistently used good

communications

and demonstrated

a safety-conscience

approach to performing

refueling operations.

Personnel

performance was excellent.

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01.3

Unit 2 Loss Of Power

LOP on 4160 V Class

1E Bus 8

a.

Ins ection Sco

e 71707

On September

17, 1997, at 3:40 a.m., a LOP occurred on Unit 2 B 4160 V Class

1E bus (PBB-SO4).

The inspector was in the control room when the event occurred

and observed

operations

personnel

respond to the event.

Unit 2 was in the

Cycle 7 refueling outage with the full core offloaded to the spent fuel pool (SFP).

b.

Observations

and Findin s

At approximately 3;40 a.m. on September

17, 1997, an emergency safety features

actuation, specifically a LOP actuation, occurred on Bus PBB-S04.

The licensee's

preliminary investigations indicated that the apparent cause of the LOP was a failure

in Load Sequencer

B, which resulted in a load shed signal to Bus B. Prior to the

event, Bus PBB-SO4 had been declared inoperable for maintenance,

but was still

energized.

Diesel Generator

B had been properly removed from service under a

clearance for scheduled

maintenance

and did not start.

Once the event occurred, the operators entered Abnormal Procedure 40AO-9ZZ12,

'Degraded

Electrical Power," Revision 1. The operations staff exhibited good

oversight and direction of activities in the control room during the event.

During the event the inspectors verified that the SFP was being adequately. cooled

by Train A of the spent fuel pool cooling (SFPC) system, since the full core was

being stored in the SFP.

An auxiliary operator was tasked with monitoring the SFP

temperature.

During the preliminary investigation, the SFP temperature

increased

approximately 3.5 'F, but was well below the established

limit.

On September

17, at 10:35 a.m., the PBB-SO4 bus was reenergized.

At 11 a.m.

the licensee started SFPC Pump B in parallel with SFPC Pump A to reduce SPF

temperature.

The licensee initiated Condition Report/Disposition Request

(CRDR) 2-7-0320 to

address this issue.

The cause of the event was still under investigation by the

licensee at the close of this inspection period.

c.

Conclusions

In response

to the unexpected

LOP to the PBB-SO4 4160V Class

1E bus on

September

17, 1997,.the control room operations staff responded

in an excellent

manner.

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01 4

Unit 2 Midloo

0 eration

Inade

uate Shutdown Coolin

Flow

1

Ins ection Sco

e 71707

On October 6, 1997, while conducting

a draindown of the Unit 2 RCS to the

midloop condition, operators suspended

the draindown after noticing an

unacceptable

deviation between Channels A and B of the RWLIS. An NRC

inspector observed the evolution.

b.

Observations

and Findin s

Control room operators were conducting

a draindown to midloop condition to

support removal of the SG nozzle dams.

The actual draindown evolution was

controlled by an additional SRO assigned to control only the draindown.

While

conducting the draindown, operators noted

a discrepancy between Channels A and

B of the RWLIS. The discrepancy of approximately 8 inches was discovered while

the wide range level indication was still in use.

The SRO in charge of the draindown

stopped the procedure just prior to entering the midloop condition and requested

that the level discrepancy

be solved before resuming the draindown.

Unit 2 was in

shutdown cooling with Train B containment spray pump in service.

Troubleshooting

the problem determined that the shutdown cooling warmup bypass Valve SIBUV690

was cracked open.

This allowed approximately 400 gpm of shutdown cooling flow

to bypass the core and flow back to the suction of the inservice shutdown cooling

pump.

Since shutdown cooling flow is measured

upstream of the bypass line,

there was no indication to the operators that actual flow to the core was low.

Actual shutdown cooling flow has an effect on water level measurement.

Since

actual shutdown cooling flow was less than indicated flow, this caused the use of

an incorrect error correction factor in determining water level. The use of the

incorrect error correction factor accounted for the difference between

Levels A and

B. At 8 p.m. on October 5, shutdown cooling flow had been lowered to what was

indicated to be just above the Technical Specification (TS) limit. With about 400

gpm of flow bypassing the core, actual flow'to the core dropped to less than the

3,780 gpm required by TS 3/4.4.1.4.2.

This condition was corrected at

approximately noon on October 6, 1997, when the shutdown cooling bypass valve

was fully shut and an operator increased shutdown cooling flow to above the TS

limit. Since this evolution was being conducted

near the end of the outage with a

newly refueled core, the decay heat load was minimal and no adverse affects were

noted due to the lower flow. After resolution of the level indication problem, the

draindown and entry into midloop operation were completed without further

roblems

p

'I

Unit 2 TS 3/4.4.1.4.2 requires that shutdown cooling flow to the core be

maintain'ed greater than 3,780 gpm.

From approximately 8 p.m. on October 5 until

approximately noon on October 6, shutdown cooling flow to the Unit 2 reactor was

less than required.

The failure to maintain greater than 3,780 gpm shutdown

cooling flow to was a violation of TS 3/4.4.1.4.2 (Violation 50-529/9716-01).

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C.

Conclusions

On October-6, 1997, the Unit 2 reactor was drained to the cold midloop condition.

A dedicated

midloop operating crew augmented

the normal operating crew during

the evolution.

During the draindown,

a discrepancy between Channels A and B of

RWLIS was discovered, which was caused

by an open shutdown cooling bypass

valve.

This resulted in less than 3780 gpm of flow through the core, a violation of

TS 3/4.4.1.4.2.

Operator oversight and direction of, the evolution and decisions to

take conservative actions related to the discrepancy observed with reactor level

measurement

were excellent,

Immediate corrective actions were timely.

08

Miscellaneous Operations Issues (92901)

08.1

Closed

LER 50-530 95-002-00:

plant operation in excess of 3800 MW thermal.

This item was described

in NRC Inspection Report 50-528,529,530/95-18

and was

dispositioned

as NCV 50-530/95018-01,

Blowdown System Misalignment Leads To

Operation Above 100'percent.

This item is closed.

08.2

Closed

LER 50-528 95-002-01:

accident analysis failed to consider shutdown

margin.

This item was described

in NRC Inspection Report 50-528,529,530/97-11

and was dispositioned

as a NCV 50-528,529,530/97011-02,

Violation of Criterion

III of Appendix B to 10 CFR Part 50. This item is closed.

08.3

Closed

Violation 50-528 96-16-01:

failure to follow the RCS drain down

procedure.

The inspectors verified the corrective actions described

in the licensee's

response

letter, dated January 3, 1997, to be acceptable

and complete.

No similar

problems were identified.

II. Maintenance

M1

Conduct of Maintenance

M1.1

General Comments on Maintenance Activities

a.

Ins ection Sco

e 62707

The inspectors observed

all or portions of the following work activities:

Clearance 97-01636:

WO 786054:

70TI-9SP03:

31 MT-9DG01:

42OP-2DG01:

LPSI Flow Control to RC 2A Containment Isolation

Diesel Engine Emergency Generator,

Unit 2

Chemical Passivation

Of Spray Pond Piping, Revision

1

Diesel Engine Surveillance Inspection, Revision 15, Unit 2

Emergency Diesel Generator A, Revision 24, Unit 2

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b.

Observations

and Findin s

The inspectors found the work performed under these activities to be professional

and thorough.

All work observed was performed with the work package present

and in active use.

Technicians were experienced

and knowledgeable of their

assigned tasks.

M1.2

General Comments on Surveillance Activities

a.

Ins ection Sco

e 61726

The inspectors observed

all or portions of the following surveillance activities:

32ST-9PE01:

18 Month Surveillance Test Of Diesel Generator

40OP-9SI01:

Shutdown Cooling Initiation

40ST-9RC01:

RCS and Pressurizer

Heatup and Cooldown Rates 4.4.8.1.1,

4.4.8.2.1

and 4.4.8.2.2.

40OP-9ZZ11:

Mode Change Checklist

b.

Observations

and Findin s

The inspectors found these surveillances were performed acceptably and as

specified by applicable procedures.

M1.3

Conclusions

on Conduct of Maintenance

and Surveillance Activities

Routine maintenance

and surveillance activities were generally conducted

in a

safety conscious manner by knowledgeable

technicians using current procedures.

M2

Maintenance and Material Condition for Facilities and Equipment

M2.1

Unit 2 Containment Closeout Ins ection

62707

On October 10, 1997, the inspectors performed

a containment closeout inspection.

Prior to entry into containment the inspectors reviewed completed

Procedure 40ST-9ZZ09, Containment Cleanliness Inspection, Revision 0. The

procedure performed

a final closeout of containment prior to Mode 4 entry.

A

thorough list of equipment to be left in containment through entry into Mode 3 was

provided to the inspectors.

The inspectors identified small miscellaneous

debris, but

no major items outside of the licensee's list were identified.

Radiation protection

personnel

removed the debris from the containment,

The items were not of

sufficient size or quantity to affect the operability of the containment emergency

sumps.

No active boric acid leaks were identified.

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Maintenance Procedures

and Documentation

SG Nozzle Dam Installation

Unit 2

Ins ection Sco

e 62707

The inspectors reviewed activities associated

with the SG nozzle dam installation;

Procedures

31MT-9RC48, "SG Nozzle Dam Installation and Removal," Revision 15,

and Procedure

30DP-OWM2, "Housekeeping

and System Cleanliness,"

Revision 1,

and personnel training records for Zone III workers.

In addition, the inspectors

discussed

system cleanliness with maintenance

department managers.

Observations

and Findin s

The inspectors reviewed Procedure 31MT-9RC48 used to install the SG nozzle

dams.

On September

9, 1997, the inspectors observed that the procedure was

detailed and properly performed.

In addition, the inspector reviewed

Procedure

30DP-OWM2 to verify proper FME controls were in place for personnel

and equipment that entered and exited the SG.

The inspector noted that a sticklight

that was used in the nozzle dam installation was not recorded on the Zone III

material and tool access

log for entering and exiting the SG

1 cold leg until

September

17. The inspectors questioned

the individual making the late entry and

the'individual indicated that they observed the sticklight enter and exit the SG

manway during the nozzle dam installation and added the line entry to ensure

completeness

of the log.

The inspectors questioned

the licensee about the FME process for the SG nozzle

dam installation.

The licensee indicated that the FME responsible

person observed

the activity from across

a table on a video monitor and did not have a headset

on

for communicating with personnel entering the SG.

The licensee has since provided

communication improvements for the FME responsible

person. The inspectors

further questioned

the licensee about the adequacy of the location of the FME

responsible

person since the person did not observe and record a sticklight entering

or exiting the SG.

The licensee interviewed the personnel

involved in the SG nozzle

dam installation and identified that the FME responsible

person did not have an

optimal view of the items entering and exiting the SG.

However, in conjunction

with the additional FME trained personnel

present and the procedural controls in the

nozzle dam installation procedure,

proper FME controls were maintained.

The

licensee concluded that the FME responsible

person not observing the sticklight

enter and exit the SG was an isolated event and did not warrant a change to the

FME program.

The inspector agreed with the licensee's conclusions.

The inspectors reviewed the training records of all the personnel that crossed the

Zone III boundary and entered the SGs.

The inspector observed that the training

records for all individuals were current.

The inspectors observed that the

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Procedure 31MT-9RC48 specifically directed the installation and removal of the

sticklight and the nozzle dam installers recalled taking the sticklight into and out of

the SG.

The inspectors concluded that the licensee complied with Procedure

30DP-OWM2

since all material that entered

and exited the SG was observed,

accounted for, and

documented

of the log sheet, although the sticklight was not logged at the time of

the work.

Conclusions

The licensee installed SG nozzle dams in the Unit 2 SG during the Cycle 7 refueling

outage to support eddy current testing of the SG tubes.

The licensee did not

provide the FME responsible

person the viewing point and communication tools to

properly monitor all items entering and exiting the SG Zone III area;

a weakness that

has since been corrected.

However, the licensee's

SG nozzle dam installation

procedure

and FME training provided'o the nozzle dam installers ensured that

acceptable

FME practices were maintained.

Maintenance Staff Knowledge and Performance

Miscalibration of RWLIS Instrumentation

Unit 2

Ins ection Sco

e 61726

On September 8, 1997, the inspectors observed control room and ISC technicians

respond to RWLIS level error indications during draining of the RCS to establish

midloop conditions.

The inspectors examined IRC troubleshooting

activities and

calibration records.

The inspectors

also witnessed the recalibration of the RWLIS

instrumentation.

Observations

and Findin s

During the draining procedure the midloop operations'crew

observed

RWLIS remain

constant at a level above that which was expected.

Indicated RWLIS level was

holding at 103 feet 8 inches with RCS letdown of 130 gpm.

This condition is

normally experienced

at the 103 foot

1 inch level, when RWLIS water level reaches

the top of the RCS hotlegs and the SG tubes begin to drain into the RCS.

The control room staff stopped draining operations

and equalized charging and

letdown flow. The midloop coordinator held a briefing to discuss the disparity

between indicated RWLIS level and where known RWLIS should have been.

IRC

was contacted

and reviewed the calibration records of the RWLIS level transmitters.

The midloop coordinator discussed

with the control room staff the possible causes

of the level deviation.

Upon review of the level transmitter calibrations records, lhC

believed that a possible maintenance

and test equipment (MRTE) error could have

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been introduced during the calibrations of the level transmitters in that all four level

transmitters were found to have as-found readings out of tolerance,

and were all

recalibrated with the same MME.

The inspectors accompanied

the ISC technicians into containment

and observed

them recalibrate one of the RWLIS level transmitters,

in accordance

with

Procedure 36MT-2RC03, "Refueling Water Level Indicating System Instrumentation

Calibration-Train A," Revision 6. The transmitter's as-found valUes were found to

be out of tolerance.

The ISC technicians recalibrated

all four level transmitters.

The licensee initiated CRDR 2-7-0301 to document the problem and determine the

root cause and transportability of the error.

The licensee's

CRDR evaluation initiated a human performance evaluation that

determined that the 8 inch RWLIS level deviation was a human performance

error.

In subsequent

efforts to determine the cause of the problem, the technicians who

performed the original calibrations r'ealized they had not opened the level transmitter

cell vent plugs as required by Procedures

36MT-2RC03/04, Steps 4.16.4.4 and

4.18.4.4.

Venting of the transmitter cell would have allowed the draining of water

in the line between the cell and the 3-way valve manifold where the M&TE was

connected.

This condition allowed the instruments to indicate approximately

8 inches high.

The licensee's

initial corrective actions included positive coaching of the IKC

technicians

on procedural compliance and attention to detail, and the issuance of a

newsflash

IS.C communication

t'o section and department

leaders describing the

event. 'The licensee is planning to revise the maintenance

test procedures to

separate

the procedure

steps into two specific actions and add a note in the

procedure to compare readings with other transmitters for calibration comparisons.

The licensee will also add this event into the next Industry Event" Training for IRC.

This licensee-identified

and corrected violation is being treated as a noncited

violation, consistent with Section VII.B.1 of the NRC Enforcement

Policy (50-528/97016-02).

Conclusions

When calibrating the RWLIS detectors to support the Unit 2, Cycle 7, refueling

outage, ISC personnel failed to adhere to procedural guidance.

This resulted in a

non-conservative

eight inch error in reactor water level indication.

This noncited

violation of procedures

represents

poor work practices by the technicians.

The

licensee's corrective actions w'ere sufficiently complete and thorough.

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III. En ineerin

E1

Conduct Of Engineering

E1.1

Shutdown Coolin

SFP

S lit Flow Test

Unit 2

a.

Ins ection Sco

e 37551

On September

10, 1997, the inspectors observed the control room operators

and

the Engineering Department perform Procedure 70TP-9PC01, "Temporary Procedure

For Evaluating Cross Tie Between Shutdown Cooling and Spent Pool Cooling,"

Revision OA. The inspectors

also reviewed calculation 13-MC-PC-217, "Shutdown

Cooling System Augmentation of the Fuel Pool Cooling-HX Performance,"

Revision 1, and the associated

10 CFR 50.59 screening

and evaluation.

b.

Observations

and Findin s

The inspectors observed

all or portions of the split flow test conducted to evaluate

the effectiveness of the shutdown cooling (SDC) to the SFP and refueling pool

lineup.

The licensee's

design basis calculation 13-MC-PC-217 questioned

the ability

of the SFPC system to remove heat under specific refueling conditions.

The split

flow test was conducted to collect data needed to evaluate the effectiveness of the

lineup.

The licensee's

UFSAR discusses

the ability of the SDC system to backup the SFPC

system.

During refueling outages

one train of SDC is normally removed from

service for maintenance.

To meet the commitment in the UFSAR, the operating

train of SDC will be required to cool the fuel in the reactor vessel and supplement

the SFPC system.

The licensee's calculation 13-MC-PC-217, Revision 1, indicates

the current SDC and SFPC systems can perform the function of keeping the SPF

temperature below the UFSAR limits.

Temporary Procedure

70PT-9PC01, was conservatively conducted

by the licensee

to validate this alignment and the design calculation.

The results of the split flow

test concluded that the licensee's

engineering calculations were correct.

The

licensee's

10 CFR 50.59 screening

and evaluation was complete and thorough.

The inspectors attended the licensee's sensitive issues briefing. The briefing was

thorough and encouraged

open communications

between all work groups.

C.

Conclusions

The engineering department

performed an accurate calculation and generated

a

good temporary procedure to verify the adequacy of the SDC system to cool the

fuel in the reactor vessel and supplement the SFPC system,

as required in the

UFSAR. Although calculations indicated performance of this test was unnecessary,

-1 1-

the licensee's

decision to verify the calculations through performance of the test

was a good example of conservative plant operations.

IV. Plant Su

ort

R1

Radiological Protection and Chemistry Controls

R1.1

General Comments

71750

The inspectors observed

radiation protection (RP) personnel,

including supervisors,

,routinely touring the radiologically controlled areas.

Licensee personnel working in

radiologically controlled areas exhibited good radiation work practices.

Contaminated

areas and high radiation areas were properly posted.

Area surveys

posted outside rooms were current.

The inspectors checked

a sample of doors,

required to be locked for the purpose of RP, and all were in accordance with

requirements.

The Unit 2, Cycle 7, refueling outage was conducted

during this inspection period.

The licensee had taken a variety of steps to keep radiation exposure to personnel

as

low as reasonably achievable.

The use of extensive planning, remote technology

and dry runs, combined with careful attention to plant operations

and chemistry

control, helped keep radiation doses during the outage to an all time low for the

site.

R4

Staff Knowledge and Performance

R4.1

Reactor Vessel Core Su

ort Barrel

Removal

Unit 2

a.

Ins ection Sco

e 71750

62707

The inspectors reviewed Procedure

31MT-9RC34, "Reactor Vessel Core Support

Barrel Removal and Installation," Revision 0, attended

RP and core barrel prejob

'riefings,

and discussed

the liftwith RP and Maintenance

personnel.

b.

Observations

and Findin s

On September

15, 1997, the inspectors attended

a prejob briefing for the first core

barrel liftfor the 10 year inservice inspection of the reactor vessel.

The briefing

included guidance for communications

(emphasizing

closed loop communications),

contingency actions, and a discussion of previous industry events.

The inspectors performed

a walkdown of containment

and observed the setup for

the evolution.

The licensee positioned several cameras to observe the evolution

from a remote station inside containment

and used telemetric dosimetry to monitor

i

-1 2-

radiation levels.

The licensee performed

a "dry-run" with the personnel involved in

the evolution to verify communication capabilities and proper equipment operation.

On September

17, the inspectors attended

a RP brief for the core barrel removal.

The licensee emphasized

the potential radiological hazards of the job and the

methods that RP would use to control access to containment

and the locked high

radiation areas that this evolution would create.

C.

Conclusions

The licensee removed the Unit 2 core barrel during the Cycle 7 refueling outage for

the 10 year inservice inspection.

The licensee's thorough planning, coordination of

activities, and training of personnel resulted in a successful

removal of the core

support barrel from the reactor vessel with minimal radiation exposure to personnel.

The licensee's activities to ensure that radiation dose rates remained low were

excellent.

V. Mana ement Meetin

s

X1

Exit Meeting Summary

The inspectors presented

the inspection results to members of licensee management

at the conclusion of the inspection on October 15, 1997.

The licensee

acknowledged the findings presented.

The inspectors

asked the licensee whether any material examined during the

inspection should be considered

proprietary.

No proprietary information was

identified.

~ ATTACHMENT 1

PARTIAL LIST OF PERSONS CONTACTED

Licensee

D. Fan, Section Leader, System Engineering

R. Fullmer, Director, Nuclear Assurance

J. Hesser, Director, Design Engineering

and Projects

D. Kanitz, Engineer, Nuclear Regulatory Affairs

A. Krainik, Department Leader, Nuclear Regulatory Affairs

D. Mautdin, Director, Maintenance

T. Radke, Director, Outages

J. Scott, Director, Site Chemistry

M. Shea, Director, Radiation Protection.

D. Smith, Director, Operations

J. Taylor, Unit 3 Operations Department Leader

C. Zell, Senior Engineer, Nuclear Regulatory Affairs

-2-

INSPECTION PROCEDURES USED

37551

60710

61726

62707

71707

71750

92901

Onsite Engineering

Refueling Activities-

Surveillance Observations

Maintenance

Observations

Plant Operations

Plant Support Activities

Plant Operations Follow-up

ITEMS OPENED

CLOSED AND DISCUSSED

~Oened

50-529/97-1 6-01

VIO

failure to maintain at least the minimum shutdown cooling

flow required by TS

50-529/97-16-02

NCV

miscalibration of RWLIS instrumentation

Closed

50-530/95002-00

LER

plant operation in excess of 3800 MW thermal

50-528/95002-01

LER

accident analysis failed to consider shutdown margin

50-528/96-16-01

VIO

failure to follow RCS drain down procedure

50-529/97-16-02

NCV

miscalibration of RWLIS instrumentation

II

-3-

LIST OF ACRONYMS USED

CRDR

FME

IRC

LOP

MME

RCS

RP

RWLIS

SDC

SFP

SFPC

SG

SRO

TS

UFSAR

condition report/disposition request

Foreign Material Exclusion

instrumentation

and controls

loss of power

maintenance

and test equipment

reactor coolant system

radiation protection

refueling water level indication system

shutdown cooling

spent fuel pool

spent fuel pool cooling

steam generator

senior reactor operator

Technical Specification

Updated Final Safety Analysis Report

f

i

I