ML17313A907

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Insp Repts 50-528/99-04,50-529/99-04 & 50-530/99-04 on 990207-0320.Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support
ML17313A907
Person / Time
Site: Palo Verde  
Issue date: 04/29/1999
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML17313A906 List:
References
50-528-99-04, 50-528-99-4, 50-529-99-04, 50-529-99-4, 50-530-99-04, 50-530-99-4, NUDOCS 9905040294
Download: ML17313A907 (38)


See also: IR 05000528/1999004

Text

e

ENCLOSURE

U.S. NUCLEAR REGULATORYCOMMISSION

REGION IV

Docket Nos.:

License Nos.:

Report No.:

Licensee:

Facility:

Location:

Dates:

Inspectors:

Approved By:

50-528

50-529

50-530

NPF-41

NPF-51

NPF-74

50-528/99-04

50-529/99-04

50-530/99-04

Arizona Public Service Company

Palo Verde Nuclear Generating Station, Units 1, 2, and 3

5951 S. Wintersburg Road

Tonopah, Arizona

February 7 through March 20, 1999

J. H. Moorman, III, Senior Resident Inspector

D. R. Carter, Resident Inspector

N. L. Saigado, Resident Inspector

G. W. Johnston, Senior Project Engineer

P. Harrell, Chief, Project Branch D

ATTACHMENT: Supplemental Information

0

9905040294

990429

PDR

ADOCK 05000528

9

PDR

EXECUTIVE SUMMARY

Palo Verde Nuclear Generating Station, Units 1, 2, and 3

NRC Inspection Report No. 50-528/99-04; 50-529/99-04; 50-530/99-04

~Oerations

~

Misdiagnosis of plant conditions and unnecessarily hurried operator actions in response

to a failure in the main turbine electrohydraulic control system caused a Unit 1 reactor

trip on high pressurizer pressure.

Posttrip operator actions were good (Section 04.1).

~

A violation of Technical Specification 4.5.2.d.3 was identified for the failure to perform

the required surveillance test on the trisodium phosphate baskets.

This Severity

Level IVviolation is being treated as a noncited violation per the guidance provided in

Appendix C of the Enforcement Policy. This issue is in the licensee's corrective action

program as Condition Report/Disposition Request 9-8-Q047 (Section 08.1).

Maintenance

Observable material condition of the three units was good. During a posttrip walkdown

of the Unit 1 containment, the licensee discovered a moderate amount of boron crystals

on carbon steel components of Reactor Coolant Pump 2A. The licensee's actions to

address the boron accumulation were good (Section M2.1).

The licensee failed to take actions to ensure that a deficient condition was appropriately

corrected on all affected components.

As a result, the deficiency was not corrected for

all turbine-driven auxiliary feedwater pumps in all units. This deficiency was identified

again by an overspeed trip of the Unit 2 turbine-driven auxiliary feedwater pump. This is

a violation of 10 CFR Part 50, Appendix B, Criterion XVI. This Severity Level IV

violation is being treated as a noncited violation consistent with Appendix C of the NRC

Enforcement Policy. The licensee took prompt actions to assess

transportibility and

correct the conditions. This issue is in the licensee's corrective action program as

Condition Report/Disposition Request 2-9-0019 (Section M3.1).

The licensee failed to provide sufficient design basis information in the appropriate

procedures.

As a result, missing and/or loose bolts were identified on the Units 1,2,

and 3 emergency diesel generator air-start headers.

The torque value for the bolts was

increased from 25 to 50 foot-pounds, and the bolts that required torqueing were not

identified in the appropriate maintenance instructions.

This is a violation of 10 CFR Part 50, Appendix B, Criterion III, for not implementing design basis information. This

Severity Level IVviolation is being treated as a noncited violation consistent with

Appendix C of the NRC Enforcement Policy. This issue is in the licensee's corrective

action program as Condition Report/Disposition Request 3-9-0026.

During routine testing of a containment isolation valve for the hydrogen control system,

the valve failed to function, as designed.

The failure was caused by the valve wiring

being improperly installed following maintenance.

The condition was not detected by

postmaintenance

testing because

the procedure, which specified the testing

requirements for the valve actuators, was inadequate.

This is a violation of 10 CFR

-2-

Part 50 Appendix B, Criterion XI; however, this Severity Level IVviolation is being

treated as a noncited violation, consistent with Appendix C of the NRC Enforcement

Policy. This issue is in the licensee's corrective action plan as Condition

Report/Disposition Request 3-9-0010 (Section M4.1).

~

Inattention to detail led to a failure to followprocedures while retrieving and verifying

replacement 480-Vac circuit breakers.

This resulted in the installation of two

nonsafety-related circuit breakers into safety-related motor control center cubicles

affecting two high pressure safety injection valves. This is a violation of Technical

Specification 5A.1 for the failure to followprocedures.

Postwork reviews also failed to

prevent the discrepancies.

This Severity Level IVviolation is being treated as a

noncited violation, consistent with Appendix C of the NRC Enforcement Policy. This

issue is in the licensee's corrective action program as Condition Report/Disposition

Request 1-9-0030 (Section M4.2).

~En ineerin

r

A Y2K readiness plan had been developed and was being implemented by the licensee.

The plan was organized and contained the necessary elements to address current and

potential problems from the Y2Kbug. A Y2Kcontingency plan has been developed, but

not finalized. The licensee was well positioned to complete Y2K remediation prior to the

end of the year (Section E1.1).

A violation of Criterion!II was identified for not specifying the correct type of seal fittings

for conduits.

As a result, during flooding of a portion of the auxiliary building, water

entered the conduits. This affected the operability of safety-related equipment.

This

Severity Level IVviolation is being treated as a noncited violation consistent with

Appendix C of the enforcement policy. This issue is in the licensee's corrective action

program as Condition Report/Disposition Request 1-60236 (Section E8.2).

~

The radiological protection program was effectively implemented in those areas

reviewed (Section R1.1).

e

l

Re ort Details

Summa

of Plant Status

Unit 1 operated at 100 percent power until March 10, 1999. The unit experienced a reactor trip

on high pressurizer pressure.

See Section 04.1 for details. The unit was returned to

100 percent power on March 15, 1999, and remained at that power level for the duration of this

inspection period.

Units 2 operated at 100 percent power until March 19, 1999, at which time the unit began a

coastdown for the planned eighth refueling outage.

Unit 3 operated at essentially 100 percent power for the duration of this inspection period.

04

Operator Knowledge and Performance

04.1

-Reactor Tri

Due to Hi h Pressurizer Pressure

Unit 1

a.

Ins ection Sco

e 71707 93702

On March 10, 1999, at 1:26 p.m., the Unit 1 reactor tripped from 100 percent power on a

valid high pressurizer pressure signal. The inspectors responded to the control room to

observe operator actions and assess

plant conditions. The inspectors also conducted

interviews with operators and reviewed personnel statements and the printout of alarms.

b.

Observations and Findin s

The Unit 1 reactor was operating at 100 percent power when a failure in the throttle

pressure limiter circuit of the main turbine electrohydraulic system caused all turbine

control valves to stroke shut over an approximately 6 second period. Both the steam

bypass control system (SBCS) and the reactor power cutback (RPCB) system properly

responded by opening the steam bypass valves. The secondary operator observed that

the steam bypass valves were open and reported this to the crew. In the span of

approximately 6 seconds,

the control room supervisor (CRS) erroneously diagnosed that

the valves were open due to a failure of the SBCS and directed the secondary operator

to shut all steam bypass valves using Emergency Off Switch HS-1010.

The secondary

operator responded promptly to the order by the CRS, after a cursory review of plant

parameters.

When all steam bypass valves went shut, some of the main steam safety

valves lifted and reseated.

This transient resulted in a high pressurizer pressure reactor

trip. A short time after the reactor trip, the SBCS was returned to automatic.

The

operators responded to the reactor trip by using the correct procedures, and they

appropriately classified the trip as uncomplicated.

Approximately 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> after the trip, a timer card in the steam generator (SG) level

control circuitry failed. This caused the economizer feedwater control valve to SG B to

open slightly. Despite operator actions to isolate feedwater to the SG, level increased to

the high SG level main steam isolation signal setpoint.

After the main'steam isolation

f

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signal setpoint was reached, the operators continued the plant cooldown by using the

atmospheric dump valves.

The operators successfully stabilized the plant in Mode 3 at

normal operating pressure and temperature.

From review of personal statements taken from the shift crew and the control room

alarm printout, the inspectors determined that the initial diagnosis was conducted in the

first few seconds of the transient without observation of turbine load or control

valve'osition.

Although the operators looked for the RPCB, the decision to take the SBCS to

emergency off was made just prior to receiving the RPCB alarm.

Lowering turbine load

and control valve position was not observed by either the control room supervisor or the

secondary operator prior to making the diagnosis.

These indications would have

confirmed to the operators that the SBCS was functioning properly in response to

closure of the control valves. The inspectors determined that operator response to the

transient was conducted without the proper diagnosis, unnecessarily hurried, and

inappropriate for plant conditions at the time. The licensee was further assessing

operator performance through a formal human performance evaluation to determine

how the event willbe incorporated into operator training.

C.

Conclusions

Misdiagnosis of plant conditions and unnecessarily hurried operator actions in response

to a failure in the main turbine electrohydraulic control system caused a Unit 1 reactor

trip on high pressurizer pressure.

Posttrip operator actions were good.

08

Miscellaneous Operations issues (92901)

08.1

Closed

Licensed Event Re ort LER 50-529/98-001:

Surveillance Test Deficiency

Found During Quality Assurance Audit Leads to Technical Specification (TS) 3.0.3/4.0.3

Entry.

On March 1, 1998, Unit 2 control room personnel declared both trains of the emergency

core cooling system inoperable due to exceeding, the specified 18 month surveillance

interval of TS Surveillance Requirement (SR) 4.5.2.d.3, "ph of Trisodium Phosphate,"

pIus the maximum allowable extension of 25 percent.

The licensee entered limiting

condition for operation TS 3.0.3 and invoked the provisions of TS SR 4.0.3 to allow up to

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> to permit the completion of the missed surveillance.

The licensee satisfactorily

completed TS SR 4.5.2.d.3 analysis within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> and exited TS limiting condition'for

operation TS 3.0.3.

The failure to perform the SR within its required interval is a violation of TS 4.5.2.d.3.

This Severity Level IVviolation is being treated as a noncited violation, consistent with

Appendix C of the NRC Enforcement Policy. This violation is in the licensee's corrective

action program as condition report/disposition request (CRDR) 9-8-Q047

(50-29/9904-01).

-3-

Conclusions

A violation of TS 4.5.2.d.3 was identified for the failure to perform the required

surveillance test on the trisodium phosphate baskets.

This Severity Level IVviolation is

being issued as a noncited violation per the guidance provided in Appendix C of the

Enforcement Policy. This issue is in the licensee's corrective action program as

Condition Report/Disposition Request 9-8-Q047.

08.2

Closed

LER 50-530/99-001:

Loss of Automatic Closure of Containment Isolation

Valve (CIV)

This LER was issued to discuss the events described in Section M4.1 of this report.

II. Maintenance

M1

Conduct of Maintenance

M1.1

General Comments on Maintenance Activities Units 2 and 3

a.

Ins ection Sco

e 62707

The inspectors observed all or portions follwing activities performed per the listed work

document:

874321

"Troubleshoot and Rework the Problem With Valve 2JSIBUV0659

Stroking Slow" (Unit 2)

823838

"Perform 6 Month Inspection of Charging Pump A" (Unit 3)

856616

"Replace Charging Pump A Suction and Discharge Valves" (Unit 3)

b.

Observations and Findin s

The inspectors found the work performed under these activities to be properly

performed.

Allwork observed was performed with the work package present an in

active use. Work and foreign material exclusion practices observed were good.

Technicians were experienced and knowledgeable of their assigned tasks.

C.

Conclusions

Knowledgeable technicians used approved procedures to perform routine maintenance

activities in a safety conscious manner.

Good work and foreign material control

practices were observed.

I

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M1.2

General Comments on Surveillance Activities Units 2 and 3

a.

Ins ection Sco

e 61726

The inspectors observed all or portions of the following activities performed per the

listed surveillance procedures:

33ST-9HJ01

"Control Room AFU Air Flow Capacity and Pressurization Test,"

Revision 5 (Unit 2)

73ST-9AF02

"AFA-P01 - Inservice Test," Revision 10 (Unit 2)

36ST-9SA02

"ESFAS Train B Subgroup Relay Functional Test," Revision 19 (Unit 3)

b.

Observations and Findin s

The inspectors found that knowledgeable personnel performed these surveillances

satisfactorily, as specified by applicable procedures.

c.

Conclusions

Knowledgeable technicians used approved procedures to conduct surveillance activities

in a satisfactory manner.

M2

Maintenance and Material Condition of Facilities and Equipment

M2.1

Review of Material Condition Durin

Plant Tours

Units 1 2 and 3

a.

Ins ection Sco

e 62707

During this inspection period, routine tours of all units were conducted to evaluate plant

material condition. The inspectors also reviewed the licensee's assessment

of boric

acid accumulation on Unit 1 Reactor Coolant Pump 2A.

C

b.

Observations and Findin s

Observations of plant material condition during this inspection period identified no major

observable material condition deficiencies.

Minor deficiencies brought to the attention of

the licensee were documented with work requests.

The licensee conducted a posttrip walkdown of the Unit 1 containment to assess

the

reactor coolant system for boron accumulation that would result from minor system

leaks. This walkdown revealed that a moderate amount of boron crystals had formed on

Reactor Coolant Pump 2A. The boron was on the bolted joint between the reactor

coolant pump seal housing adapter (commonly known as the "top hat") and the seal

housing.

There was also a large quantity of boric acid buildup on the stainless steel

seal housing surface, carbon steel clamp ring, and main closure nuts. The licensee

determined that the leakage that led to the boric acid precipitation was approximately

~

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e

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4 drops per second from the "top hat" of the reactor coolant pump seal. After the boric

acid had been cleaned off of the components, an inspection was conducted to assess

the components for wastage.

The inspection revealed some wastage of the carbon

steel components.

The amount of corrosion was assessed

by the licensee, and it was

determined that the structural integrity of the clamp ring and main closure nuts was not

affected.

The condition was documented and dispositioned in deficiency Work Order

(WO) 874896 and CRDR 9-9-0326.

The inspectors reviewed the licensee's assessment

and agreed with the conclusions.

Conclusions

Observable material condition of the three units was good.

During a posttrip walkdown

of the Unit 1 containment, the licensee discovered a moderate amount of boron on

carbon steel components of Reactor Coolant Pump 2A. The licensee',s actions to

address the boron accumulation were good.

M3

Maintenance Procedures and Documentation

M3.1

Auxilia

Feedwater

AFW Pum

Turbine Overs

eed

Units1 2 and 3

Ins ection Sco

e 62707

On February 18, 1999, during postmaintenance

testing of AFW Pump A, the pump

turbine tripped on overspeed.

The inspectors evaluated the licensees response to the

turbine trip, conducted interviews with the system engineer, and reviewed related

documentation.

Observations and Findin s

On February 17, the licensee declared AFW system Train A inoperable to perform

planned maintenance on Valves AFA-HV33and AFA-UV37, discharge valves to SG 2B.

On February 18, the licensee operated AFW Pump A in accordance with Surveillance

Procedure 73ST-9AF02, "AFA-P01-Inservice Test," Revision 10, to perform

postmaintenance

testing for Valves AFA-HV33and AFA-UV37. After approximately

19 minutes of operation, AFW Pump A reached the electrical overspeed setpoint and

tripped.

The pump was quarantined for root cause investigation, and the licensee initiated

CRDR 2-9-0019 to document and evaluate the cause of the pump trip. The licensee

initiated WO 872823 to troubleshoot the cause of the overspeed.

Investigation of the

turbine control system by mechanics found that the governor linkage had an

approximate 1/4-inch gap between the governor linkage fork clevis and the spring seats

that are attached to the governor valve stem.

Valve stem position is controlled via a pivoted linkage fork that connects the valve stem

to a remote servomechanism.

The governor valve stem is prevented from rotating by an

antirotation block threaded onto it and held in place by a set screw. The governor

linkage fork clevis fits over the antirotation block and is held onto the valve stem by a set

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of spring seats on either side of it. The spring seats were threaded onto the valve stem

and held in place by a set screw. A 0.010- to 0.015-inch clearance is required to be

maintained between the linkage fork clevis and the spring seats.

The additional 1/4-inch clearance resulted in the remote Servomechanism

being able to

travel its full length and bottom out before the governor valve could fullyseat to control

turbine speed.

As steam quality improved with turbine operation, the governor valve

could not be closed enough to compensate for the increased efficiency: This resulted in

a gradual increase in turbine speed over a 3-minute period prior to the trip.

The licensee postulated that the excessive clearance could have resulted if: (1) both

the antirotation block and the inner spring seat set screws were either not sufficiently

tightened or had worked loose, allowing the antirotation block and inner spring seat to

change their location on the valve steam, (2) steam flow eddy currents within the

governor valve caused the valve plug and stem to rotate, and (3) the outer spring seat

remained firmlysecured to the stem.

A similar event was documented on Field Change Request (FCR) 65.359-M, dated

October 1983.

In this event, loose set screws on the Unit 1 AFW Pump A turbine

governor inner spring seat allowed the valve stem to turn. This resulted in

uncontrollable excessive turbine speed.

The FCR corrective actions added a second

set screw to the inner spring seat and required the spring seats to be lockwired

together.

During the Unit 2 refueling outage in September 1997, WO 795078 directed the

performance of Maintenance Instruction (Ml) MAF-00008, "Disassemble/Inspect

Turbine

Governor Valve." This procedure did not contain steps to tighten set screws for the

spring seats or reference that two set screws were required.

The procedure did not

provide instructions to lockwire the spring seats together, but did have a step to tighten

the set screw on the antirotation block. The inspectors determined that FCR 2235

corrective actions were never incorporated into all affected plant maintenance

instructions.

The licensee inspected the turbine governor valves on the turbine-driven AFW pumps

for all three units. The outer spring seat on the Units 1, 2, and 3 valves had one set

screw, and only the inner spring seat on the Unit 2 valve had two set screws.

None of

the spring seats in any unit were lockwired. Spring seat clearances

in Units 1 and 3

were inspected and found to have the correct clearance between the linkage fork clevis

and the spring seats.

Set screws in the Units 1 and 3 spring seats were tight. The

licensee had replaced the turbine governor valves on Units 1 and 3 in 1992 and 1994,

respectively.

When the governor valves were replaced, the updated design information

was not applied to the new valves. This resulted in the governor valve spring seats

being installed without two set screws.

The failure to incorporate FCR 2235 actions into maintenance instructions and to

maintain design control measures commensurate

with those applied to the modified

design is a violation of 10 CFR Part 50, Appendix B, Criterion III, "Design Control." This

Severity Level IVviolation is being treated as a noncited violation, consistent with

Appendix C of the NRC Enforcement Policy. This violation is in the licensee's corrective

action program as CRDR 2-9-0019 (50-528,-529,-530/9904-02).

\\

-7-

Conclusions

The licensee failed to take actions to ensure that a deficient condition was appropriately

corrected on all affected components.

As a result, the deficiency was not corrected for

all turbine-driven auxiliary feedwater pumps in all units. This deficiency was identified

again by an overspeed trip of the Unit 2 turbine-driven auxiliary feedwater pump. This is

a violation of 10 CFR Part 50, Appendix B, Criterion XVI. This Severity Level IV

violation is being treated as a noncited violation consistent with Appendix C of the NRC

Enforcement Policy. The licensee took prompt actions to assess

transportibility and

correct the conditions.

This issue is in the licensee's corrective action program as

Condition Report/Disposition Request 2-9-0019.

Emer enc

Diesel Generator

EDG Air-Start Manifold Bolts Not Pro erl Tor ued

Units1

2 and3

Ins ection Sco

e 62707

On February 18, 1999, during a routine surveillance, the licensee identified loose and

missing bolts on the Unit 3 EDG A air-start manifold. The inspectors evaluated the

circumstances surrounding the loose and missing bolts, conducted interviews with the

system engineer, and reviewed documentation related to the event.

Observations and Findin s

During performance of Surveillance Procedure 40ST-9DG01, "Diesel Generator A Test,"

Revision 6, an auxiliary operator noted that, of the two bolts holding the air-start

manifold to Cylinder 9R, one was missing and the other bolt was loose. The air-start

manifold bolts on Cylinder 7R were also loose. The licensee initiated CRDR 3-9-0026 to

document the problem and to evaluate the transportability of the issue.

Licensee

management

did not consider the EDG to be inoperable, because the EDG started

within its required time limits and the air-start header was still held in place by the other

cylinders on the right side.

Licensee inspection of all EDGs (two in each of the three

units) revealed that Unit 1 EDG A was also missing a bolt on Cylinder 3R. The licensee

initiated WRs 955623, 955638, 955639, 955640, 955641, and 955642 to verify the

torque on the air-start manifold bolts of all EDGs. All EDG manifold bolts required

tightening approximately 1/4 turn to satisfy the c'urrent specification value of 50 ft-lbs.

CRDR 1-6-0030, dated February 20, 1996, described loose and missing bolts on the

air-start manifold of several cylinders on Unit 1 EDG A and Unit 3 EDG B. An operability

determination associated

with this CRDR concluded that the EDGs remained operable

with the loose or missing bolts, due to the rigidityof the manifold and the number of

bolts that remained tight on the adjacent cylinders. The CRDR root cause determination

identified a low torque value of 25 ft-Ibs as the primary reason for the bolts becoming

loose.

In addition, the CRDR identified that, in order to remove the air-start manifold

from one of the cylinder heads for maintenance,

it was necessary to loosen the bolts on

adjacent cylinders to allow removal of the manifold flange from the head being worked.

However, this portion of the task was not in the maintenance procedure.

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CRDR 1-6-0030 immediate corrective actions included the verification and retorque of

the manifold bolts on both EDGs in all units. Long-term corrective actions included:

~

Increasing the torque value of the manifold bolts from 25 to 50 ft-lbs, and

~

Adding a step to Ml MDG-00046, "Remove and Replace Cylinder Head," to

check the torque on adjacent cylinder head air-start manifold bolts.

The licensee modified Drawing M018-519, "AirStarting Header," on May 29, 1996, to

increase the air-start manifold bolt torque value from 25 to 50 ft-lbs. However, the

licensee did not change any Mls, which mechanics use to perform maintenance on the

EDGs, to incorporate the increased torque value.

In addition, step 4.8.1A was added to

Ml MDG-00046 to torque the manifold bolts on the adjacent heads to the head being

worked. However, the licensee did not add the additional step to Ml MDG-00065,

"Piston Modification," the Ml used to remove the Cylinder 8R head on Unit 3 EDG A.

The failure to implement design basis information into appropriate procedures

is a

violation of 10 CFR Part 50, Appendix B, Criterion III. This Severity Level IVviolation is

being treated as a noncited violation, consistent with Appendix C of the NRC

Enforcement Policy. This violation is in the licensee's corrective action program as

CRDR 3-9-0026 (50-528,-529,-530/9904-03).

The inspectors also determined that Mls MDG-00046 and MDG-00065 did not contain

steps that instructed mechanics to loosen air-start manifold bolts on cylinders adjacent

to those which are to be worked. The inspectors interviewed a maintenance planner,

.who indicated that, if the adjacent manifold bolts needed to be loosened, the Ml would

be modified in the field to reflect the change.

Ml MDG-00065 used to perform work on

Unit 3 EDG A Cylinder 8R did not document the additional steps to loosen the adjacent

manifold bolts.

Licensee corrective actions detailed in CRDR 3-9-0026 included changing the Mls to

increase the torque values of the air-start manifold bolts to 50 ft-lbs, as specified on

Drawing M018-519.

In addition, steps were added to all Mls associated with EDG head,

removal to torque the adjacent cylinder air-start manifold bolts. Steps were also added

to provide for the loosening of adjacent manifold bolts to facilitate the removal of the air-

start manifold on a cylinder head requiring work. Long-term corrective actions required

Maintenance Engineering to screen and identify critical engine systems or components

that have a potential for bolts to become loose and to use this data to change

appropriate Mls. The inspectors determined that these actions were appropriate.

Conclusions

The licensee failed to provide sufficient design basis information in the appropriate

procedures.

As a result, missing and/or loose bolts were identified on the Units 1, 2,

and 3 EDG air-start headers.

The torque value for the bolts was increased from 25 to

50 ft-lbs, and the bolts that required torqueing were not identified in the appropriate

maintenance instructions. This is a violation of 10 CFR Part 50, Appendix B,

Criterion III, for not implementing design basis information. This Severity Level IV

violation is being treated as a noncited violation consistent with Appendix C of the NRC

Enforcement Policy. This issue is in the licensee's corrective action program as

Condition Report/Disposition Request 3-9-0026.

-9-

Maintenance Staff Knowledge and Performance

Loss of Automatic Closure of a CIV Unit 3

Ins ection Sco

e 62707

On January 23, 1999, the licensee identified that inboard containment hydrogen control

supply isolation Valve'3JHPAUV0001 failed to close during routine functional testing.

The inspectors reviewed the circumstances surrounding the failure of the valve to

operate properly, observed troubleshooting activities, and reviewed LER 99-001-00 and

CRDR 3-9-0010.

Observations and Findin s

On January 23, during the performance of Surveillance Procedure 36ST-9SA01,

"ESFAS Train A Subgroup Relay Functional Test," Revision 19, Valve 3JHPAUV0001

failed to close during testing of containment isolation actuation signal (CIAS) Relay

K213. The licensee initiated CRDR 3-9-0010 to document the valve failure and to

evaluate transportability of the event.

The licensee initiated WO 870644 to troubleshoot and repair the valve. Troubleshooting

revealed that the wiring for Valve HPAUV0001 was not in accordance with

Diagram 3-E-HPB-002, "Containment Hydrogen Control System Hydrogen Control

Containment Isolation Valve 3JHPAUV-1," Revision 6. The improper wiring

configuration not only prevented the valve from closing on a CIAS but, in the as-found

configuration, the valve would have opened on a CIAS. This represented

a partial loss

of the ability to isolate containment.

The wiring was returned to the proper configuration

and the licensee successfully completed Surveillance Procedures 73ST-9XI08, "HC 8

HP Valves - Inservice Test," Revision 2, and 36ST-9SA01 and then declared Valve

3HPAUV0001 operable.

The licensee's investigation determined that on September 24, 1998, during the Unit 3

refueling outage, WO 834623 required the actuator for Valve 3JHPAUV0001 to be

removed for static diagnostic testing per Procedure 32MT-9ZZ56, "Motor Operator

Testing Using MOVATS3500 System," Revision 20. When wiring was removed from

the actuator, Wire 52, which was removed from Terminal 20, was documented on the

determination/retermination sheet as having been removed from Terminal 21. During

reassembly of the actuator on September 26, Wire 52 was reianded per the

determination/retermination

sheet on the wrong terminal (Terminal 21 instead of 20). A

second party verification was conducted, as required by plant procedures, for both the

determination and retermination of all wiring associated

with the actuator maintenance.

The licensee also determined that the wire was configured correctly prior to this

maintenance by successful performance of Surveillance Procedure 36ST-9SA01,

completed on August 2, 1998, and Procedure 73ST-3DG01, "Class 1E Diesel Generator

and Integrated Safeguards Surveillance Test - Train A," Revision 8, completed on

September 21, 1998.

Both surveillances ensured that the entire actuation circuit

operated properly.

f

e

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The retest of the valve specified by WO 834623 was a full-stroke test per

Procedure 32MT-9ZZ49, '-'PM Inspection of Rotork Operators," and a local leak rate test.

These tests functionally verified operation of the valve, but did not test the CIAS portion

of the engineered safeguards feature actuation signal (ESFAS) actuation circuitry. Had

either Surveillance Procedure 36ST-9SA01 or 73ST-3DG01 been identified as a retest,

the wiring error would have been identified.

The licensee determined, as part of CRDR 3-9-0010 root cause determination, that only

Rotork type motor-operated valve actuators are susceptible to having the safety function

disabled during actuator maintenance.

Unique to the 20 Rotork actuators installed in

the three units was the issue of hammering (cyclically energizing/deenergizing

the valve

into its seat) due to the CIAS being a locked in signal. To ensure that the hammering

did not occur for Rotork actuators, the ESFAS control wiring was routed directly to the

actuator, and a limitswitch contact was put in series with the ESFAS actuation to

interrupt the main ESFAS signal prior to seating the valve. The licensee determined

that only 20 valves with Rotork actuators would require ESFAS functional testing after

actuator maintenance.

A review of the test history found that Valves 1JHPBUV002 and

3JHPBUV002 had maintenance performed without a proper ESFAS retest.

The

licensee performed Surveillance Procedure 36ST-9SA01 on the two valves in question,

and both were found to be operable.

Valve 3JHPAUV0001 was incorrectly rewired during maintenance, and this condition

was not detected by the required maintenance

retest.

The valve was inoperable from

September 29, 1998, through January 23, 1999, during which it could not perform its

automatic isolation function. The failure to include adequate

retest requirements in

Procedure 39DP-9ZZ04 for Rotork-type valve actuators is a violation of 10 CFR Part 50,

Appendix B, Criterion XI. This Severity Level IVviolation is being treated as a noncited

violation, consistent with Appendix C of the NRC Enforcement Policy. This violation is in

the licensee's corrective action program as CRDR 3-9-0010

(50-528,-529,-530/9904-04).

c.

Conclusions

During routine testing of a CIV for the hydrogen control system, the valve failed to

function as designed.

The failure was caused by the valve wiring being improperly

installed following maintanance.

The condition was not detected by postmaintenance

testing because

the procedure, which specified the testing requirements, was

inadequate.

This is a violation of 10 CFR Part 50 Appendix B, Criterion XI, for not

performing adequate testing of a valve. This Severity Level IVviolation is being treated

as a noncited violation, consistent with Appendix C of the NRC Enforcement Policy.

This issue is in the licensee's corrective action program as Condition Report/Disposition

Request 3-9-0010.

e

M4.2

Nonsafe

-Related Circuit Breakers Installed In Safe

-Related A

lications Unit 1

a.

Ins ection Sco

e 71707 37551

62707

On February 19, 1999, the licensee identified two nonsafety-related circuit breakers

installed in 480-Vac safety-related Motor Control Center (MCC) Cubicles 1EPHBM3417

and 1EPHBM3419 for high pressure safety injection (HPSI) Valves 1JSIBUV616 and

1JSIBUV636. The inspectors reviewed applicable logs, WOs, procedures, and

CRDR 1-9-0030.

b.

Observations and Findin s

On February 19, a procurement engineer identified, while conducting a routine audit of a

quarterly failure data trending report, that two nonsafety-related circuit breakers were

possibly installed in two safety-related MCC cubicles.

As documented

in the unit logs,

Valves 1JSIBUV616 and 1JSIBUV636 were deenergized to verify breaker qualification.

The inspectors verified that operators had entered TS 3.6.3 Condition A for CIVs and

TS 3.5.3 Condition B for HPSI B. Once the licensee confirmed the discrepancies, WO 872905 was generated and implemented to replace the nonsafety-related

breakers.

The licensee's evaluation of the affect on the safety function of the two HPSI valves

during the time that the nonsafety-related breakers were installed, indicated that the

breakers would have performed their required design function for the following reasons:

~

Overcurrent protection requirements were tested by Procedure 32MT-9ZZ74.

~

MCC cubicles were located in an area classified as a mild environment.

~

Southern California Edison performed seismic tests on the breakers, which

indicated that the breakers remained functional during and after the tests.

Also,

structural integrity of the breakers was verified after the seismic tests.

In March 1998, the licensee performed Plant Change Work Orders 803385 and 803397,

which changed the overload heaters and reset the breakers installed in MCC

Cubicles 1EPHBM3417 and 1EPHBM3419. The existing breakers failed to trip within

the allowed time per Procedure 32MT-9ZZ74, "Molded Case Circuit Breaker Test,"

Revision 14. The licensee initiated Maintenance Instruction Work Orders (MIWO)

834070 and 834067 to procure and test the new breakers.

It was during the

performance of these MIWOs that the licensee incorporated the wrong replacement

parts.

The failure to followprocedures for retrieving and verifying proper replacement parts, as

described in the equipment list associated

with MIWOs 834070 and 834067, is a

violation of TS 5.4.1. This Severity Level IVviolation is being treated as a noncited

violation, consistent with Appendix C of NRC Enforcement Policy. This violation is in the

licensee's corrective action program as CRDR 1-9-0030 (50-528,-529,-530/9904-05).

4

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Completed MIWOs 834070 and 834067 documented the nonsafety-related equipment

identification numbers on several steps.

Thorough postwork reviews would have

provided a second barrier to identify and prevent these discrepancies.

The inspectors

assessed

that the postwork reviews performed for both MIWOs as poor.

The inspectors considered the storage of nonsafety- and safety-related equipment in the

Level B electrical storage area as a contributing factor. The maintenance personnel

retrieved the incorrect replacement breakers from this storage area in Unit 2. While the

storage facilitywas acceptablly maintained per plant procedures, the licensee

subsequently determined that this storage area would only store nonsafety-related

components.

The licensee initiated six WOs to inspect all safety-related MCC cubicles in all units to

verify installation of the proper breakers.

At the conclusion of this inspection period, the

licensee had inspected approximately 50 percent of the MCC cubicles without identifying

any additional discrepancies.

c.

Conclusions

Inattention to detail led to a failure to followprocedures while retrieving and verifying

replacement 480-Vac circuit breakers.

This resulted in the installation of two

nonsafety-related, circuit breakers into safety-related MCC cubicles affecting two high

pressure safety injection valves. This is a violation of TS 5.4.1 for the failure to follow

procedures.

Postwork reviews also failed to prevent the discrepancies.

This Severity

Level IVviolation is being treated as a noncited violation, consistent with Appendix C of

the NRC Enforcement Policy. This issue is in the licensee's corrective action program

as Condition Report/Disposition Request 1-9-0030.

M8.1

Closed

Ins ection Followu

Item 50-528 -529 -530/9812-05:

Fire potential in the

Emergency Diesel Generator rooms.

The inspections performed an in-office review of this item and determined that no

additional inspection was required since the item was captured by the licensee's

condition reporting program as Condition Report/Disposition Request 98-0267.

E1

Conduct of Engineeriag

E1.1

Year 2000 Y2K Readiness

Units 1 2 and 3

a.

Ins ection Sco

e 37551

On February 24, 1999, the inspectors met with personnel responsible for implementing

the Y2K Readiness

Plan to determine if progress was being made in efforts to cope with

the Y2K computer bug. The inspectors reviewed procedures and documentation of the

program status and held discussions with licensee personnel.

e

-13-

b.

Observations and Findin s

The inspectors determined that the Y2K Readiness

Plan was being implemented by a

dedicated Y2K Project Manager, who reports directly to the Vice President of Nuclear

Engineering.

The Y2K Project Manager was supported by a Y2K Core Team, as well as

other station personnel who were assigned collateral Y2K duties for their departments.

The inspectors determined that the Y2K project had adequate

resources and sufficient

management support to accomplish the Y2K program.

The inspectors reviewed, "Year 2000 Readiness

Plan for the Palo Verde Nuclear

Generating Station," Revision 3. This document defined the roles and responsibilities of

the personnel involved with the Y2K program and contained the guidelines for the

implementation plan. The inspectors determined that the licensee had a well planned

approach to Y2K readiness.

The inspectors verified that the licensee had developed a

contingency plan, although at the time of the inspection, the plan was not finalized.

The inspectors reviewed the completion status of the Y2Kprogram. The inventory,

assessment,

and remediation planning steps were 100 percent complete.

The licensee

was approximately 42 percent complete in remediation of department and

information-technology supported systems and was approximately 94 percent complete

in remediation of embedded systems.

The inspectors determined that the licensee was

well positioned to complete Y2K remediation.

c.

Conclusions

A Y2K Readiness

Plan had been developed and was being implemented by the

licensee.

The plan was organized and contained the necessary elements to address

current and potential problems from the Y2K bug. A Y2K contingency plan had been

developed, but not finalized. The licensee was well positioned to complete Y2K

remediation prior to the end of the year.

E8

Miscellaneous Engineering Issues (92903)

E8.1

Closed

Violation VIO 50-528 50-529 50-530/9617-02:

Failure to Implement Work

Instructions.

This violation involved the failure of plant personnel to reference Piping Installation

Specification 13-PN-304 during installation of a modification to the essential chilled

water system chillers.

The modification was intended to reduce the overcooling of the essential chilled water

system condensers

in the winter, when low essential cooling water temperatures

and

system loading have resulted in low condenser pressure.

During the installation, a

pressure control valve was the final component installed to complete the piping portion

of the modification. The valve was installed using bolted flange connections.

Downstream of the pressure control valve was an elbow, followed by a box-style hanger.

Upstream of the pressure control valve was a piping tee with one end going to the

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bypass valve and the other end going to a flanged connection to the chiller. The bolted

flange connection, when installed, would have resulted in cold spring of the piping,

causing stress in a hanger and the piping. Specification 13-'PN-204 stated that all

situations involving cold spring should be evaluated by engineering.

Design engineering initiated CRDR 9-6-1371 to evaluate this concern.

An estimate

determined that bolting the flanges would provide roughly 0.1 inches of spring.

The

calculated additional stress that would be added to the hanger, the additional

stress'dded

to the piping, and any impact this condition had on the response to a seismic

event and to expected thermal expansion and contraction corresponded

to roughly half

of the code allowable initial stress limits. The inspectors determined that completion of

corrective actions by the licensee to address CRDR 9-6-1371 were satisfactorily

accomplished.

E8.2

Closed

LER 50-528 -529 -530/97-003:

Construction Design Deficiency Resulted in

Inadequate Protection Against Floodwater Migration

On September 22, 1996, while in Mode 5, an overfillof an SG resulted in flooding on the

100-foot elevation of th'e main steam support structure (MSSS). Inspections of the

80-foot elevation found some electrical junction boxes with water present inside. The

cause of the leakage was determined to be from the submergence

of Erickson fittings in

conduits leading from the 100-foot elevation to the 80-foot elevation in the MSSS.

Investigation by engineering personnel revealed that, unless specifically ordered as

such, Erickson fittings are not designed to be watertight. The licensee further

determined that, with a maximum worst case feedwater line break, a height of 8.65 feet

could be reached in the MSSS. The flooding during the steam generator overfill event

reached a height of approximately 6 inches.

Testing of an Erickson fitting flooded to a

height of 8.65 feet resulted in a leakage rate of 6.8 quarts in 10 minutes.

Engineering

concluded that the Trains A and B AFW pumps would not have been able to perform

their intended safety function if a design basis flooding event had occurred.

Having

determined that the potential existed during a design basis flooding event for water

leakage to migrate to lower elevations through conduit, the licensee initiated

CRDR 1-6-0236 and conducted a survey to identify all possible leakage paths from

conduits throughout the three units. As a result, all identified Erickson fittings below

projected flood heights in the MSSS, diesel generator, auxiliary, and control buildings in

all three units were sealed.

Further, 14 other conduit fittings that required a seal to be

installed were identified. The inspectors determined this review adequately addressed

, the transportability of the design deficiency to all the units and buildings.

Electrical equipment qualification requirements for submergence

are addressed

in

10 CFR 50.49(e)(6).

Two guidance documents were referenced by the regulation,

"Guidelines for Evaluating Environmental Qualification of Class 1E Electrical Equipment

in Operating Reactors," November 1979 (DOR Guidelines), and NUREG-0588, "Interim

Staff Position on Environmental Qualification of Safety-Related Electrical Equipment."

10 CFR Part 50, Appendix B, Criteria III, requires the adequacy of design be verified by

-15-

the performance of design reviews. Contrary to these requirements, the licensee had

not verified by design review or by another method, such as testing, the adequacy of

conduit penetrating flooding barriers to resist water intrusion. This resulted in the

potential for rendering the redundant trains of AFW unavailable following a design basis

flooding event in the MSSS.

This Severity Level IVviolation of Criterion Ill is being treated as a noncited violation,

consistent with Appendix C of the NRC Enforcement Policy. This violation is in the

licensee's corrective action program as CRDR 1-60236 (50-528,-529,-530/9904-05).

Conclusions

A violation of Criterion lil was identified for not specifying the correct type of seal fittings

for conduits. As a result, during flooding of a portion of the auxiliary building, water

entered the conduits.

This affected the operability of safety-related equipment.

This

Severity Level IVviolation is being treated as a noncited violation consistent with

Appendix C of the enforcement policy. This issue is in the licensee's corrective action

program as Condition Report/Disposition Request 1-60236.

IV. Plant Su

ort

R1

Radiological Protection and Chemistry Controls

R1.1

General Comments on Radioio ical Protection Controls Units 1 2 and 3

a.

Ins ection Sco

e 71750

The inspectors monitored radiological protection activities during routine site tours.

b.

Observations and Findin s

I

The inspectors observed radiation protection personnel, including supervisors, routinely

touring the radiologically controlled areas.

Licensee personnel working in radiologically

controlled areas exhibited good radiation work practices.

Contaminated areas and high radiation areas were properly posted.

Area surveys

posted outside the room were current. The inspectors checked a sample of doors,

required to be locked for the purpose of radiation protection, and all were in accordance

with requirements.

C.

Conclusions

The radiological protection program was effectively implemented in those areas

reviewed.

w

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V. Mana ement Meetin s

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee's staff at the

conclusion of the inspection on March 25, 1999. The licensee acknowledged the

findings presented.

The inspectors informed the licensee that some material'examined during the inspection

was considered proprietary.

ATTACHMENT

PARTIALLIST OF PERSONS CONTACTED

Licensee

P. Brandjes, Department Leader, Electrical Maintenance Engineering

F. Gowers, Site Representative,

El Paso Electric

J. Hesser, Director, Engineering

R. Henry, Site Representative,

Salt River Project

W. Ide, Vice President, Nuclear Engineering

S. Jones, Section Leader, Engineering Systems

D. Kanitz, Engineer, Nuclear Regulatory Affairs

P. Kirker, Unit 3 Department Leader, Operations

A. Krainik, Department Leader, Nuclear Regulatory Affairs

J. Levine, Senior Vice President, Nuclear

D. Marks, Section Leader, Nuclear Regulatory Affairs

G. Overbeck, Vice President, Nuclear Production

T. Radke, Director, Outages

G. Shanker, Department Leader, Speciality Engineering

D. Smith, Director, Operations

M. Sontag, Section Leader, Nuclear Assurance

E. Sterling, Department Leader, Nuclear Assurance

S. Terrigrino, Manager, Strategic Communications

P. Wiley, Unit 2 Department Leader, Operations

INSPECTION PROCEDURES USED

37551

61726

62707

71707

71750

92901

93702

92903

Onsite Engineering

Surveillance Observations

Maintenance Observations

Plant Operations

Plant Support Activities

Plant Operations Followup

Event Followup

Engineering Followup

~Oened

50-529/9904-01

50-528,-529,

-530/9904-02

50-528,-529,

-530/9904-03

50-528,-529,

-530/9904-04

NCV

NCV

NCV

NCV

-2-

ITEMS OPENED AND CLOSED

Missed 18-month surveillance of trisodium phosphate baskets

(Section 08.1)

Failure to correct a deficient condition in the auxiliary

feedwater pump governors (Section M3.1)

Failure to provide sufficient instructions for torqueing the EDG

air-start header bolts (Section M3.2)

Inadequate postmaintenance

testing of valve actuators

(Section M4.1)

50-528,-529,

-530/9904-05

50-528,-529,

-530/9904-06

Closed

50-529/98-001

50-530/99-001

50-529/9904-01

50-528,-529,

-530/9904-02

50-528,-529,

-530/9904-03

50-528,-529,

-530/9904-04

50-528, -529,

-530/9812-05

50-528,-529,

-530/9904-05

NCV

Failure to followprocedure for identification of correct

replacement parts (Section M4.2)

NCV

Failure to conduct an adequate design review of conduit

penetrating flooding barriers (Section E8.2)

LER

Surveillance Test Deficiency Found During QA Audit Lead to

TS 3.0.3/4.0.3 Entry (Section 08.1 )

LER

Loss of Automatic Closure of a CIV (Section 08.2)

NCV

Missed 18-month surveillance of trisodium phosphate baskets

(Section 08.1)

NCV

Failure to correct a deficient condition in the auxiliary

feedwater pump governors (Section M3.1)

NCV

Failure to correct a deficient condition for torqueing the EDG

air-start header bolts (Section M3.2)

NCV

Inadequate postmaintenance

testing of valve actuations

(Section M4.1)

IFI

Fire potential in diesel rooms (Section M8.1-)

NCV

Failure to followprocedure for identification of correct

replacement parts (Section M4.2)

50-528,-529,

-530/9904-06

50-528,-529,

-530/9617-02

NCV

VIO

Failure to conduct an adequate design review of conduit

seals in flood areas (Section E8.2)

Failure to Implement Work Instructions for a Modification

(Section E8.1)

50-528,-529,

-530/97-003

LER

Construction Design Deficiency Resulted in Inadequate

Protection Against Floodwater Migration (Section E8.2)

I

1

-3-

LIST OF ACRONYMS USED

AFW

CFR

CIAS

CIV

CRDR

CRS

EDG

ESFAS

FCR

ft-Ibs

HPSI

IFI

LER

MCC

Ml

MIWO

MSSS

NCV

NRC

PDR

RPCB

SBCS

SG

SR

TS

VIO

WO

Y2K

auxiliary feedwater

Code of Federal Regulations

containment isolation actuation signal

containment isolation valve

condition report/disposition request

control room supervisor

emergency diesel generator

engineered safeguards feature actuation signal

field change request

foot-pounds

high pressure safety injection

inspector followup item

licensee event report

motor control center

maintenance instruction

maintenance instruction work order

main steam support structure

noncited violation

Nuclear Regulatory Commission

public document room

reactor power cutback

steam bypass control system

steam generator

surveillance requirement

Technical Specification

violation

work order

Year 2000

J

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