ML17312B717

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Insp Repts 50-528/97-22,50-529/97-22 & 50-530/97-22 on 970908-12.Violations Noted.Major Areas Inspected:Review of Licensee Response to Inadvertent Dilution of Unit 2 Sf Pool on 970812 & Assessed Evaluation of Event by Licensee
ML17312B717
Person / Time
Site: Palo Verde  Arizona Public Service icon.png
Issue date: 10/08/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML17312B715 List:
References
50-528-97-22, 50-529-97-22, 50-530-97-22, NUDOCS 9710150071
Download: ML17312B717 (25)


See also: IR 05000528/1997022

Text

ENCLOSURE 2

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket Nos.:

License Nos.:

Report No.:

Licensee:

Facility:

Location:

Dates:

Inspector:

Approved By:

50-528

50-529

50-530

NPF-41

NPF-51

NPF-74

50-528/97-22

50-529/97-22

50-530/97-22

Arizona Public Service Company

Palo Verde Nuclear Generating Station, Units 1, 2, and 3

5951 S. Wintersburg Road

Tonopah, Arizona

September 8-12, 1997

C. J. Paulk, Reactor Inspector, Maintenance

Branch

Dr.'ale A. Powers, Chief, Maintenance

Branch

Division of Reactor Safety

ATTACHMENT:

Supplemental

Information

97iOi5007i 97i008

PDR

ADOCK 05000528

G

PDR

-2-

EXECUTIVE SUMMARY

Palo Verde Nuclear Generating Station, Units 1, 2, and 3

NRC Inspection Report 50-528/97-22; 50-529/97-22; 50-530/97-22

This special inspection was conducted to review the licensee's

response

to an inadvertent

dilution of the Unit 2 spent fuel pool on August 12, 1997.

The inspection also assessed

the evaluation of the event that was performed by the licensee.

Maintenance

The licensee's

evaluation of the inadvertent dilution of the Unit 2 spent fuel pool

was thorough and of high quality (Section M8.1).

The root cause analysis conclusion and corrective actions for the inadvertent

dilution event of the Unit 2 spent fuel pool were well documented

and supported

(Section M8.1). '

lack of adequate

inter-departmental

communications

during concurrent work

activities was a large contributor to the inadvertent dilution event in the Unit 2

spent fuel pool (Section M8.1).

A work order that failed to include a requirement to prohibit fuel movement or

handling during the implementation of a modification placed additional 'challenges to

operators responding to the boron dilution event.

This inadequate

work order was

identified as a violation (Section M8.1).

jl

l

-3-

Summar

of Plant Status

Units

1 and 3 were at full power and Unit 2 was its eighth refueling outage.

II. Maintenance

M8

IVliscellaneous Maintenance Issues (92902)

M8.1

Closed

Unresolved Item 50-529 9715-04:

Inadvertent dilution of the spent fuel

pool during installation of a design modification to provide a backup air supply to

the spent fuel pool transfer canal gate.

Beckceround

On August 12, 1997, maintenance

personnel were installing a modification to add a

permanent

backup air supply to the spent fuel pool transfer canal gate seal

~

Depressurization

of both the spent fuel pool transfer canal and cask loading pit gate

seals was required to install the modification.

The spent fuel pool contained borated

water at a concentration

of approximately 4337 ppm and the adjacent cask loading

pit contained demineralized water.

Upon depressurization

of the cask loading pit

gate seal, an exchange

of water began, resulting in an inadvertent dilution of the

spent fuel pool ~

At the time of the event, two other activities were in process

in the spent fuel pool

area.

One activity was the movement of new fuel into the pool in preparation for

the outage.

The other activity was a training exercise being conducted

by radiation

protection technicians to replace the filter on a pump that had been temporarily

placed in the cask loading pit. The shift control room operating crew was aware of

the modification work and the fuel movement, but were unaware of the filter

replacement training.

Licensee personnel took immediate actions-to secure new fuel movement after an

initial boron sample taken in the area of the cask loading pit gate indicated

1767 ppm.

A spent fuel pool bulk sample was taken at the discharge of the fuel

pool cleanup pump that indicated

a boron concentration

of 3942 ppm.

Technical Specification 3.1.2.6a., which requires

a minimum boron concentration

of

4000 ppm,

was entered on declaration from the shift supervisor.

Restoration

measures

were taken and, subsequently,

the boron concentration

was returned to

4018 ppm approximately 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> after the bulk concentration was found to be

less than 4000 ppm.

Ins ection Sco

e

The purpose of this special inspection was to evaluate

the licensee's

actions taken

during the event, to review the licensee's

evaluation of this event, to review the

proposed

corrective actions, and to independently

assess

the event.

In order to

accomplish these goals, the inspector reviewed the licensee's

evaluation,

interviewed licensee personnel,

reviewed the design change package

and associated

documents

(listed in the Attachment), reviewed the event time line documented

in

the Attachment, and reviewed licensee procedures

and Technical Specifications.

b.

Observations

and Findin s

The inspector noted that the licensee's

evaluation team considered

the filter

replacement training as a planned activity; however, the activity was not on the

work schedule,

and control room operations

personriel were not aware of the

activity. The inspector also noted, as did the evaluation team, that, while each

activity was being supervised,

no one considered

the synergistic effects of three

activities being performed simultaneously.

The inspector found that the lack of

inter-departmental

communication was a major contributor to this event.

This

finding was similar to findings in other NRC inspection reports that documented

other recent events (e.g., 50-528;-529;-530/97-09

and 97-15).

The inspector observed that the work order used to perform the filter replacement

training (Work Order 00803435) was initially written as an "activity tracking only"

work order.

Also, the work order stated that the purpose was to perform a pre-

outage test on a pump in the "cast [sic] wash down pit," and that this area was to

be partially filled with water.

This work was performed the week of July 24, 1997;

however, the pump was inadvertently placed in the cask loading pit contrary to the

location specified in the work order.

The inspector noted that, since the activity

was performed under

a tracking only work order,

a hard copy of the work order was

not required.

Therefore, the radiation protection technicians performing the test did

not have hardcopy information to indicate that the pump was in a location that was

different from that prescribed

on the work order.

As dicussed later in this section,

the placement of the pump in the cask loading pit was a contributor to the dilution

event.

While the pre-outage

testing of the pump was completed

in July, the work order

remained open.

The inspector noted that this was to allow the tracking of time

spent by the radiation protection technicians for training on the pump.

The

inspector found this to be a weakness

in the licensee's work control process since

the radiation protection technicians were allowed, by procedure,

to perform

activities that were not specified on the tracking only'ork order.

After the inspector identified the wrong location for the pump testing described

in

the tracking only work order, the work order was revised to indicate that the pump

was in the cask loading pit. However, the work order remained cpen.

-5-

Technical Specification 6.8.1 requires,

in part, that written procedures

shall be

established,

implemented,

and maintained covering the applicable procedures

recommended

in Appendix A of Regulatory Guide 1.33, Revision 2, February 1978.

Regulatory Guide 1.33, Appendix A, Revision 2, Section 9, requires that

maintenance

that can affect the performance of safety-related

equipment should be

performed in accordance

with written procedures,

documented

instructions, or

drawings appropriate to the circumstances.

The inspector noted that the work

order (WO 00793132) for the implementation of the modification of the backup air

supply system did not contain a requirement that no fuel movement or handling was

allowed during the installation of the modification.

This requirement was contained

in the design change package

(DMWO 00793132, Part II, "Other Design Input

Considerations,"

Section 1, "Dismantling and Rearranging of Existing Items" ). The

inspector found that, while this omission did not contribute to the event, it created

additional challenges to the operators'esponse

to the event because

a fuel bundle

was in the process of being moved at the time the operators were informed of the

low boron concentration.

This bundle had to be placed in a safe configuration and

required. the attention of control room operators until the bundle was safely stored.

The inspector found that the failure to translate the requirement that no fuel

movement or handling was allowed during the installation of the modification to be

a violation of Technical Specification 6.8.1 (50-528;-529;-530/9722-01).

The inspector noted that, while not a contributing factor to the event, the engineer

performing the safety evaluation for the design change package

assumed

that there

would be "no credible significant driving mechanism to cause the boron dilution to

exceed this assumed

rate [35 gpm (132.5 Lpm)J." This statement was based

on

the fact that both the fuel transfer canal and the cask loading pit would be at

approximately the same level when the cask loading pit gate seal was

depressurized.

The inspector verified through review of operator logs that the two levels were

within 2 inches (5 cm) of each other at a level of approximately 137 feet 10 inches

(42 m). Because the levels were approximately equal, the only other driving force

that was expected was that resulting from the differences in densities of the two

water volumes.

The inspector reviewed a licensee calculation that was performed

after the event and determined that the driving force due to the difference in water

densities

and temperatures

was insignificant.

The inspector found that the

assumption

of no credible significant driving force to be valid, provided the

prerequisites

and requirements from the design change package were satisfied.

While licensee personnel

had not reached

a definite conclusion, they suspected

that

the force of the water being discharged

from the pump being tested in the cask

loading pit at the time the gate seal was depressurized

was enough to move the

gate and cause the flow between the two water volumes.

The inspector discussed

this theory with a licensee engineer and found the basis to be reasonable.

The

S

I

-6-

inspector found that the testing of the pump was not included in the safety

evaluation and was not accounted

for in the prerequisites.

The inspector found the licensee's evaluation of the dilution event (Root Cause

Investigation for CRDR 2-7-0259, dated August 29, 1997) thorough and of high

quality.

The conclusions

reached,

the root cause(s)

identified, and the corrective

actions proposed

were well documented

and supported.

The corrective actions

included:

the revision of the safety evaluation to address

fuel movement during the

Units

1 and 3 installation of the modification; the determination of whether or not

the cask loading pit should be filled with borated water during the installation of the

modification, or should the pit be filled indefinitely with borated water; the revision

of a calculation for determining the volume in the different areas of the spent fuel

pool; the development

of a strategy to increase

a questioning attitude about

activities in adjacent work areas;

and, the enhancement

of job briefings, in general,

and sensitive issues briefings when one or more activities are to be performed in the

spent fuel pool areas, including new fuel movement.

The recurring theme from the evaluation of poor inter-departmental

communications

was a concern.

Licensee management

stated that the communications

at the plant

did not meet their expectations.

While management's

heightened

attention to the

problem with communications was apparent

(as noted through interviews), the

actions taken to correct. the issue have not had time to be effective.

Conclusions

The licensee's

evaluation of the boron dilution event was thorough and of high

quality.

The root cause analysis conclusions

and corrective actions were well

documented

and supported.

A lack of adequate

inter-departmental

communications

during concurrent work activities was a significant contributor to the event.

An

inadequate

work order that failed to include a requirement to prohibit fuel movement

or handling during the implementation of a modification placed additional challenges

to operators

responding to the event and was identified as a violation of Technical Specification 6.8.1.

8.2

Closed

Ins ection Followu

Item 50-528 -529 -530 9601-01:

Design

requirements

for the nonessential

auxiliary feedwater system not consistently

translated.

The licensee was requested

to respond to the subject inspection report to document

a verbal commitment to clarify the licensing basis for the nonessential

auxiliary

feedwater train.

The inspector reviewed the licensee's

June 1996 letter from

Mr. W. L. Stewart to Mr. L. J. Callan.

The inspector found the letter to have adequately

addressed

the concerns that

minimum acceptable

requirements

for the auxiliary feedwate.

pumps were

substantially less than the original design capability.

The inspector noted that the

-7-

manner in which the probabilistic risk assessment

took credit for the nonsafety-

related nonessential

auxiliary feedwater system to reduce core damage frequency,

and the description of the auxiliary feedwater system in the Updated Final Safety

Analysis Report, caused confusion.

In the June 1996 letter, the licensee provided

Licensing Document Change

Request 3654 that modified the wording in the

Updated Final Safety Analysis Report to clarify the basis of the nonessential

auxiliary feedwater system.

The inspector found the licensee's

response

to have adequately

addressed

the

concerns identified in the subject report.

8.3

Closed

Ins ection Followu

Item 50-528 -529 -530 9619-0'I:

Use of ultrasonic

test block of different material than tested.

This item was reviewed in NRC Inspection Report 50-528;- 529;- 530/97-11

and

left open pending identification of the scope of the required corrective action and

the planned implementation of the corrective actions.

The inspector reviewed the

licensee's corrective actions and the schedule for implementing the actions.

The

inspector found that the scope was limited to the steam generator

nozzles which

were scheduled

to be reinspected

using an ultrasonic probe calibrated on the same

type material as being examined.

The reinspections

were appropriately scheduled

for the next refueling outage on each unit.

8.4

Closed

Violation 50-528 -529 -530 9709-01:

Procedural requirements

not met

(four examples).

The inspector verified the corrective actions described

in the licensee's

response

letter, dated June 2, 1997, to be reasonable

and complete.

No similar problems

were identified.

8.5

Closed

Violation 50-528 -529 -530/9709-02:

Provisions were not established

to

assure that the safety-related function of the gate seals would not be lost.

The inspector verified the corrective actions described

in the licensee's

response

letter, dated June 2, 1997, to be reasonable

and complete.

No similar problems

were identified..

8.6

Closed

Violation 528 -529 -530/9709-03:

Gate seal inspection procedure was

inadequate.

The inspector verified the corrective actions described

in the licensee's

response

letter, dated June

2, 1997, to be reasonable

and complete.

No similar problems

were identified.

L

-8-

V. Mana ement Meetin

s

X1

Exit Meeting Summary

The inspector presented

the inspection results to members of licensee management

at the

conclusion of the inspection on September

12, 1997.

The licensee representatives

acknowledged

the findings presented.

The inspector asked the licensee representatives

whether any materials examined during

the inspection should be considered

proprietary.

No proprietary information was identified.

ATTACHMENT

SUPPLEMENTAL INFORMATION

PARTIAL LIST OF PERSONS CONTACTED

Licensee

S. Bauer, Licensing Section Leader, Nuclear Regulatory Affairs

M. Burns, Department Leader, Design Engineering

R. Buzard, Senior Consultant,

Nuclear Regulatory Affairs

K. Farley, Senior Engineer, Design Engineering

W. Ide, Vice President,

Engineering

M. Karbassian,

Section Leader, Nuclear Engineering

J. Levine, Senior Vice President,

Nuclear

D. Marks, Section Leader, Nuclear Regulatory Affairs - Compliance

H. Mortazavi, Senior Engineer, Design Engineering

G. Overbeck, Vice President,

Nuclear Production

M. Shea, Director, Radiation Protection

D. Smith, Director, Operations

NRC

N. Salgado, Acting Senior Resident Inspector

INSPECTION PROCEDURE USED

IP 92902

Followup - Maintenance

ITEMS OPENED AND CLOSED

O~ened

50-529/9722-01

VIO

Failure to translate requirements

from design change package

to installation work order

Closed

50-528/9601-01

IFI

Design requirements for Auxiliary Feedwater

N Train Not

Consistently Translated

50-529/9601-01,

IFI

Design requirements for Auxiliary Feedwater

N Train Not

Consistently Translated

50-530/9601-01

IFI

Design requirements for Auxiliary Feedwater

N Train Not

Consistently Translated

1

-2-

50-528/9619-01

IFI

Use of Ultrasonic Test Calibration Block of Different Material

Than Tested

50-529/961 9-01

IFI

Use of Ultrasonic Test Calibration Block of Different Material

Than Tested

50-530/961 9-01

IFI

Use of Ultrasonic Test Calibration Block of Different Material

Than Tested

50-528/9709-01

VIO

Procedural Requirements

Not Met, Four Examples

50-529/9709-01

VIO

Procedural

Requirements

Not Met, Four Examples

50-530/9709-01

VIO

Procedural Requirements

Not Met, Four Examples

50-528/9709-02,

VIO

Provisions Were Not Established to Assure That the Safety-

Related Function of the Gate Seals Would Not Be Lost

50-529/9709-02

VIO

Provisions Were Not Established to Assure That the Safety-

Related Function of the Gate Seals Would Not Be Lost

50-530/9709-02

VIO

Provisions Were Not Established to Assure That the Safety-

Related Function of the Gate Seals Would Not Be Lost

50-528/9709-03

VIO

Gate Seal Inspection Procedure Was Inadequate

50-529/9709-03

VIO

Gate Seal Inspection Procedure

Was Inadequate

50-530/9709-03

VIO

Gate Seal Inspection Procedure

Was Inadequate

50-529/9715-04

URI

Inadvertent Dilution of Spent Fuel Pool

LIST OF DOCUMENTS REVIEWED

PROCEDURES

PROCEDURE

REVISION

TITLE

30DP-OAP01

30DP-OMR01

30DP-9MP01

30DP-9MT01

20

Maintenance Instruction Writer's Guide

2

Maintenance

Rule

22

Conduct of Maintenance

5

Assessment

of Risk When Performing Maintenance

'

-3-

PROCEDURE

REVISION

PROCEDURES

TITLE

30DP-9WP01

30DP-9WP02

31 MT-9IA01

31 MT-9PC02

40DP-9OP02

51DP-9OM03

78OP-9FX02

90DP-OIP03

90DP-OIP10

8

Work Identification

21

Work Document Development and Control

Installation and Removal of Temporary Air/Nitrogen for Fuel

Transfer Canal Gate

F<<el Transfer Tube. Quick Closure Device

Conduct of Shift Operations

Site Scheduling

Fuel Transfer Machine

Condition Report Screening

and Processing

Condition Reporting

OTHER DOCUMENTS

Root Cause Investigation for CRDR 2-7-0259, August 29, 1997

DMWO 00793132, Revision 1, Design Change to:

add

a permanently connected

source of

backup air supply to the fuel transfer canal gate; add seal pressure

instrumentation;

resize

the gas supply orifices; reclassify the spent fuel pool transfer canal and cask loading pit

gate seals as nonquality-related;

and reclassify the fuel transfer canal gate valve as quality-

related

Calculation 13MC-IA-306, "SFP Gate Seal Gas LK Ec BU Bottle Usage Rate Det.,"

Revision 0

Calculation 13-MC-IA-307, "Orifice and PRV Sizing for the IA System to the SFP Gate

Seals," Revision 0

Calculation 13-MC-PC-208, Appendix C, "Spent Fuel Pool Water Temperature,"

Revision 0

1L

DRAWING NUMBER

REVISION

DRAWINGS

TITLE

01-P-IAF-503

02-P-I AF-503

02-M-IAP-003, SH.

'I

02-M-IAP-003, SH. 2

02-M-IAP-003, SH.

1

02-M-IAP-003, SH. 2

02-M-PCP-001

02-M-PCP-001

03-P-IAF-503

1 3-C1 74-14

1 3-C1 74-1 5

0.00

0.00

34

34

35

35

13

0.00

10

Fuel Bldg. Unit

1 Isometric Instrument Air System

Cask Loading Pit & Fuel Transfer Canal Seal Gates

Fuel Bldg. Unit 2 Isometric Instrument Air System

Cask Loading Pit & Fuel Transfer Canal Seal Gates

P & I Diagram Instrument and Service Air System,

Sheet

1 of 2

P & I Diagram Instrument and Service Air System,

Sheet 2 of 2

P & I Diagram Instrument and Service Air System,

Sheet

1 of 2

P & I Diagram Instrument and Service Air System,

Sheet 2 of 2

P & I Diagram Fuel Pool Cooling & Cleanup System

P & I Diagram Fuel Pool Cooling & Cleanup System

Fuel Bldg. Unit 3 Isometric Instrument Air System

Cask Loading Pit & Fuel Transfer Canal Seal Gates

Spent Fuel Pool Gates Fuel Transfer Canal Gates

Spent Fuel Pool Gates Fuel Transfer Canal Gates

EVENT TIME LINE

July 24, 1997

Authorization given to perform pre-outage test on a pump in the Unit 2 cask wash down

pit in accordance

with Work Order 00803435

August 9, 1997

Cask loading pit filled to approximately 137 ft 10 in (42 m)

August 12, 1997 (all times MST)

0830

Sensitive issues briefing conducted;

boron concentration

4337 ppm

{

1

-5-

0930

1025

Late morning to 1630

1 330-1430

1520

1525

1544

1555

1600

1716

Modification work began on cask pit gate seal

Air supply to seal isolated

Filter replacement

training in cask loading pit

Existing tubing was disconnected

from seal, and the seal

depressurized;

eddy currents observed

and reported to control

room

New fuel movement commenced

Boron sample taken in vicinity of the cask loading pit gate;

concentration was 1767 ppm

Control room notified of the results of the boron sample; shift

supervisor ordered fuel handlers to stop all fuel movement and

directed chemistry to obtain a bulk sample

Fuel movement stopped (after remaining fuel assembly was

placed in a safe configuration)

Bulk sample results indicated

a boron concentration of

3942 ppm; shift supervisor entered the action statement for

Technical Specification 3.1.2.6a.

Using the time as 1544

Cask loading pit gate seal repressurized

August 13, 1997

0916

0925

1245

Fuel handling activities resumed; boron concentration

equalized

at approximately 3870 ppm (greater than the 2150 ppm

Technical Specification 3.9.13 requirement for fuel movement)

Last new fuel assembly was stored

Addition of boron initiated

August 14, 1997

1725

Boron concentration

at 4018 ppm, within Technical

Specification allowable; exited Technical Specification 3.1.2.6a. action statement