IR 05000454/2007002

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IR 05000454-07-002; 05000455-007-002; on 01/01/2007-03/31/2007; Byron Station, Units 1 and 2; Equipment Alignment and Fire Protection
ML071350661
Person / Time
Site: Byron  Constellation icon.png
Issue date: 05/15/2007
From: Richard Skokowski
NRC/RGN-III/DRP/RPB3
To: Crane C
Exelon Generation Co, Exelon Nuclear
References
IR-07-002
Download: ML071350661 (41)


Text

SUBJECT:

BYRON STATION, UNITS 1 AND 2 NRC INTEGRATED INSPECTION REPORT 05000454/2007002; 05000455/2007002

Dear Mr. Crane:

On March 31, 2007, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated inspection at your Byron Station, Units 1 and 2. The enclosed report documents the inspection findings which were discussed on April 6, 2007, with Mr. Dave Hoots and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

This report documents two NRC-identified findings of very low safety significance (Green).

One finding involved a violation of NRC requirements. In addition, one licensee-identified violation which was determined to be of very low safety significance is listed in this report.

However, because of the very low safety significance of the violations and because they were entered into your corrective action program, the NRC is treating these violations as non-cited violations (NCV) consistent with Section VI.A.1 of the NRC Enforcement Policy.

If you contest the subject or severity of a Non-Cited Violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, D.C. 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the Resident Inspector office at the Byron Station. In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter and its enclosure will be made available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRCs document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Richard A. Skokowski, Chief Branch 3 Division of Reactor Projects Docket Nos. 50-454; 50-455 License Nos. NPF-37; NPF-66 Enclosure: Inspection Report 05000454/2007002; 05000455/2007002; w/Attachment: Supplemental Information cc w/encl: Site Vice President - Byron Station Plant Manager - Byron Station Regulatory Assurance Manager - Byron Station Chief Operating Officer Senior Vice President - Nuclear Services Vice President - Operations Support Vice President - Licensing and Regulatory Affairs Director Licensing Manager Licensing - Braidwood and Byron Senior Counsel, Nuclear Document Control Desk - Licensing Assistant Attorney General Illinois Emergency Management Agency State Liaison Officer, State of Illinois State Liaison Officer, State of Wisconsin Chairman, Illinois Commerce Commission B. Quigley, Byron Station

SUMMARY OF FINDINGS

IR 05000454/2007002; 05000455/2007002; on 01/01/2007-03/31/2007; Byron Station,

Units 1 and 2; Equipment Alignment and Fire Protection.

This report covers a 3-month period of baseline resident inspection and announced baseline inspections on radiation protection and on biennial heat sink performance. These inspections were conducted by regional inspectors and the resident inspectors. Two Green findings, one of which was a non-cited violation (NCV), were identified. The significance of most findings is indicated by their color (Green, White, yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review.

NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

A. Inspector-Identified and Self-Revealed Findings

Cornerstone: Mitigating Systems

Green.

The inspectors identified a Non-Cited Violation (NCV) of the Byron Station Operating License for the failure to have adequate alternate safe shutdown procedure.

Specifically, licensees procedure BOP FR-1, Fire Response Guidelines, did not include adequate steps and instructions to prevent the draining of the refueling water storage tank (RWST) into the containment sump in the event of a fire in the auxiliary electrical equipment room (AEER) or the control room. The licensee implemented appropriate procedure changes for both the AEER and control room fire zones to isolate all potential RWST drain paths.

The finding is greater than minor because it affected the attribute of procedure quality for protection against external factors and it impacted the objective of the mitigating systems cornerstone. The failure to provide adequate instructions in the alternate shutdown procedure to promptly prevent the draining of the RWST to the containment sump could have adversely impacted the operators ability to promptly take appropriate actions and could have complicated safe shutdown in the event of a fire. The finding was of very low safety significance based on Phase 2 and Phase 3 SDP evaluations completed by the Region III senior reactor analyst (SRA) in accordance with IMC 0609, Appendix F, Fire Protection Significance Determination Process. (Section 1R05.2)

Green.

The inspectors identified a finding for the licensees failure to maintain setpoint control of the constant level oilers. Specifically, the licensee did not incorporate the vendors recommendation on setting the oil level for the essential service water pumps.

This condition increased the challenges to the proper functioning of the lubricating oil and thus to the bearings of the safety-related pumps. The licensee subsequently reset the oil level for the pumps to the recommended setting and entered this issue into their corrective action program.

This finding is more than minor because of the potential for degradation of oil and bearings to safety related components, which could adversely affect their availability and reliability. This finding is of very low safety significance because no bearings had been damaged due to the high oil levels despite operating in this condition for many years and no significant oil degradation had occurred. The inspectors did not identify a violation of regulatory requirements. However, the cause of the finding is related to the cross-cutting element of problem identification and resolution, particularly the thoroughness of the extent of condition review. (Section 1R04.2)

Licensee Identified Violations

One violation of very low safety significance, which was identified by the licensee, has been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensees corrective action program. This violation and the corrective actions are listed in Section 4OA7 of this report.

REPORT DETAILS

Summary of Plant Status

Unit 1 operated at or near full power throughout the inspection period.

Unit 2 operated at or near full power throughout the inspection period with the following exceptions:

  • On January 27, 2007, the unit reduced power to 95 percent to swap feedwater pumps.

The unit returned to full power on January 28, 2007.

  • On February 11, 2007, the unit reduced power to 94 percent to swap feedwater pumps.

The unit returned to full power on the same day.

  • On March 15, 2007, the unit entered coastdown operation.
  • On March 28, 2007, the unit reduced power from 87 to 80 percent to perform main steam safety valve testing. The unit returned to 87 percent power on March 30, 2007.

The unit was scheduled to enter a refueling outage on April 1,

REACTOR SAFETY

Cornerstone: Initiating Events, Mitigating Systems, Barrier Integrity and

Emergency Preparedness

1R04 Equipment Alignment (71111.04Q and S)

.1 Partial Walkdowns

a. Inspection Scope

The inspectors performed one partial walkdown sample of accessible portions of a train of risk-significant mitigating system equipment during times when the train was of increased importance due to the redundant trains or other related equipment being unavailable. The inspectors utilized the valve and electric breaker lineups and applicable system drawings to determine that the components were properly positioned and that support systems were lined up as needed. The inspectors also examined the material condition of the components and observed operating parameters of equipment to determine that there were no obvious deficiencies. The inspectors used the information in the appropriate sections of the Updated Final Safety Analysis Report (UFSAR) and Technical Specifications (TS) to determine the functional requirements of the systems.

The inspectors verified the alignment of the following:

The inspectors also reviewed selected issues documented in IRs, to determine if they had been properly addressed in the licensees corrective action program. The documents reviewed during this inspection are listed in the Attachment to this report.

b. Findings

No findings of significance were identified.

.2 Complete Walkdown

a. Inspection Scope

During the inspection, the inspectors finished one complete system alignment inspection of the accessible portions of the Unit 2 Train A Essential Service Water System. This system was selected because it was considered both safety-related, and risk significant for the plant condition.

In addition to the walkdowns, the inspectors reviewed the following documentation to verify that the system was properly maintained in accordance with design basis documents:

  • selected operating procedures regarding system configuration;
  • issue reports (IRs) for the system initiated within the last year.

Documents reviewed as part of this inspection are listed in the Attachment. This walkdown represented one inspection sample.

b. Findings

Introduction:

A finding of very low safety significance (Green) was identified by the inspectors for the licensee failure to maintain setpoint control of the constant level oilers.

This condition increased the challenges to the proper functioning of the lubricating oil and thus to the bearings of the safety-related pumps. This finding was of very low safety significance because no bearings had been damaged due to the high oil levels despite operating in this condition for many years and the oil had only been moderately impacted.

Description:

The inspectors observed that the constant level oilers on the four safety-related essential service water pumps (licensee system designator SX) were all above the maximum oil level line. The vendor recommended that to prevent bearing damage the maximum oil level should be at the center of the gauge glass and that it should be measured with the pump not operating. High oil levels can cause air to be pushed into the oil resulting in frothing, and thinning of the oil, which can cause inadequate heat removal and bearing damage. The licensee wrote IRs 555893 and 555201 to address the inspectors observations.

After reviewing the issue, the licensee acknowledged the potential to damage the pump bearings due to either high oil levels or oil thinning. However the licensee did not identify any instances of bearing damage that could be attributed to improper oil levels.

The oil levels in the SX motors were all immediately reduced to within the vendor recommended levels. The licensees corrective actions included communications with the vendor to better understand the need to maintain the oil level at the center of the gauge glass, revising work instructions to ensure the oil level was restored to within the required range following maintenance and working with the equipment operators to ensure they understood the need to limit oil level.

Analysis:

The inspectors determined that the failure to have setpoint control of the safety-related constant level oilers was a performance deficiency warranting a significance evaluation in accordance with Inspection Manual Chapter (IMC) 0612, Power Reactor Inspection Reports, Appendix B, Issue Disposition Screening, issued November 2, 2006. This finding was more than minor because of the potential for degradation of oil/bearings to safety-related components that would increase their unavailability and unreliability and could have affected the core decay heat removal system.

In accordance with IMC 0609, Significance Determination Process, issued November 22, 2005, Appendix A, Determining the Significance of Reactor Inspection Findings for At-Power Situations, issued March 23, 2007, Attachment 1, the inspectors determined that this finding screened as Green. Specifically, the finding did not result in a loss of operability, did not result in a loss of system safety function, did not result in an actual loss of safety function of a single train for greater than its TS Allowed Outage Time, did not represent an actual loss of safety function of one or more non-TS trains of equipment designated as risk-significant for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> and was not related to a seismic, flooding or severe weather initiating events. Therefore, the inspectors concluded that this finding was of very low safety significance (Green).

(FIN 05000454/2007002-01; 05000455/2007002-01)

This finding has a cross-cutting aspect in the area of problem identification and resolution because the licensee failed to thoroughly evaluate a similar problem such that extent of condition was considered and the cause was resolved. That past problem was described in NRC Inspection Report 05000454/455/2006005.

Enforcement:

The inspectors concluded that no violation of regulatory requirements had occurred as there was no procedure requirement in the maintenance work packages to check or adjust the constant level oiler setpoints; no significant oil degradation had occurred; and no bearings had been damaged due to the lack of setpoint control.

1R05 Fire Protection

.1 Quarterly Walkdowns

a. Inspection Scope

The inspectors conducted fire protection walkdowns that were focused on availability, accessibility, and the condition of fire fighting equipment; the control of transient combustibles and ignition sources; and on the condition and operating status of installed fire barriers. The inspectors reviewed applicable portions of the Byron Station Fire Protection Report and selected fire areas for inspection based on their overall contribution to internal fire risk, as documented in the Individual Plant Examination of External Events Report.

The inspectors verified that fire hoses and extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were unobstructed; that transient material loading was within the analyzed limits; and that fire doors, dampers, and penetration seals appeared to be in satisfactory condition.

The Byron Station Pre-Fire Plans applicable for each area inspected were used by the inspectors to determine approximate locations of firefighting equipment.

The inspectors completed seven inspection samples by examining the plant areas listed below to observe conditions related to fire protection:

  • Unit 2 Containment Pipe Penetration Area Elevation 364' (Zone 11.3-2);
  • Unit 2 Division 22 Miscellaneous Electrical Equipment Room (Zone 5.4-2);
  • Auxiliary Building elevation 346' general area (Zone 11.2-0);
  • Auxiliary Building Elevation 401' General Area (Zone 11.5-0);
  • Auxiliary Equipment Electric Room (Zone 5.5-1);
  • Diesel Generator and Day Tank Room Unit 1 Train A (Zone 9.2-1); and
  • Diesel Fuel Oil Storage Tank Room Unit 1 Train A (Zone 10.2-1).

The inspectors reviewed selected issues documented in IRs, to determine if they had been properly addressed in the licensees corrective action program. The inspectors also verified that minor issues identified during the inspection were entered into the licensees corrective action program. The documents reviewed during this inspection are listed in the Attachment to this report.

b. Findings

No findings of significance were identified.

.2 Tri-ennial Fire Protection

a. Adequacy of Safe Shutdown Procedures to Address Draining of the RWST

Introduction:

The inspectors identified a Non-Cited Violation (NCV) of the Byron Station Operating License having very low safety significance (Green) for inadequate alternate safe shutdown procedures. Specifically, licensees Procedure BOP FR-1, Fire Response Guidelines, did not include adequate steps/instructions to prevent the draining of the refueling water storage tank (RWST) into the containment sump in the event of a fire in the auxiliary electrical equipment room (AEER) or the control room.

Description:

Unresolved Item (URI 05000454/2004005-03; 05000455/2004005-03) was opened during the 2004 triennial fire protection inspection regarding the adequacy of alternate safe shutdown procedures in the event of a fire in the AEER or the control room. Specifically, the inspectors questioned the adequacy of Procedure BOP FR-1 to ensure safe shutdown in the event of a fire in any of these areas that could result in the spurious opening of one of the low pressure safety injection containment sump supply isolation valves, 1SI8811A, and 1SI8811B. The licensees safe shutdown (SSD)analysis documented that for a fire in either area, diagnostic indication, including RWST level and containment sump level circuits, may not be available. This issue was considered as an unresolved item pending NRC review of associated circuit issues. On December 20, 2005, the NRC issued Regulatory Issue Summary (RIS) 2005-30, Clarification of Post-Fire Safe-Shutdown Circuit Regulatory Requirements, clarifying the NRC staff position, on protecting equipment affected by hot shorts, that cables whose fire-induced failure could cause maloperation of redundant trains in a III.G.2 area due to hot shorts must be protected. Based on the inspectors review of the Byron Safety Evaluation Reports (SERs) and Fire Protection Report (FPR), and the information provided by RIS 2005-30, the inspectors determined that the spurious opening of one of these valves, 1SI8811A or 1SI8811B was credible and the licensees procedures should have adequately addressed this concern.

35 of Procedure BOP FR-1, Revision 6 (revision which was available during the 2004 inspection), addressed operator actions required for a fire in the AEER area.

A table listing valves that may spuriously operate was provided in Step 13 of the

. The instructions were to send an operator to open the breaker for SI8811A/B and verify the valve position locally. The information that the RWST inventory can drain to the sump was provided in the same instruction but no further procedural guidance was provided regarding the use of the sump and emergency core cooling system pumps to maintain hot standby and proceed to cold shutdown as stated in the SSD analysis. Similar instructions/discussion also applied to Attachment 38 for a fire in the control room.

During the 2004 inspection, the licensee indicated that in the event that the RWST drained to the containment sump, operators would use Procedure 1BEP ES-1.3, Transfer to Cold Leg Recirculation, Unit 1, to maintain safe shutdown. The inspectors found that this procedure relied upon the use of indications and controls in the control room which may not be available in the event of a fire in the AEER or control room. For example, the procedure instructed operators to verify adequate containment sump level using level indicators 1LI-PC006 and 1LI-PC007. However, these instruments may not be available during this postulated fire. In addition, this procedure relied upon aligning the residual heat removal (RHR) pumps suction to the containment sump. The SSD analysis showed that both RHR pumps had control cables present in the AEER and control room fire areas. Credit was taken for repairing the control cables for one of the RHR pumps per existing repair procedure.

Based on the above discussion, the inspectors determined that the licensee did not have adequate procedures for alternate shutdown fire areas to ensure safe shutdown in the event of a fire in the AEER or the control room. Attachments 35 and 38 of Procedure BOP FR-1 did not provide adequate instructions to promptly prevent the draining of the RWST to the containment sump. Procedure 1BEP ES-1.3 relied upon the use of indication and controls that may not be available in the event of a fire.

Since the inspection in 2004, the licensee revised Procedure BOP FR-1 for both the AEER and control room fire zones. The licensee added steps earlier in the procedure to promptly assure that an adequate RWST inventory was maintained. The steps included instructions for the operators to de-energize both valves SI8811A/B and to verify valves were in the closed position. The steps also provided instructions, that in the event any one of these valves was found not closed, for operators to close its associated SI8812A/B valve and one of the following valves RH8716A, RH8716B, or opposite train valve SI8812A/B to isolate all potential drainage.

Analysis:

The inspectors determined that the failure to provide adequate steps/instructions in alternate shutdown Procedure BOP FR-1 (Revision 6) to ensure safe shutdown in the event of a fire in the AEER or control room was a performance deficiency, warranting a significance evaluation. Specifically, Attachments 35 and 38 of Procedure BOP FR-1 did not provide adequate instructions to promptly prevent the draining of the RWST to containment sump. The inspectors concluded that the finding was more than minor in accordance with IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue Screening, issued on November 2, 2006. The finding involved the attribute of procedure quality for protection against external factors (i.e., fire) because the failure to provide adequate instructions in alternate shutdown procedure to promptly prevent the draining of the RWST to the containment sump could have adversely impacted the operators ability to promptly take appropriate actions and could have complicated safe shutdown in the event of a fire. As such, this finding affected the mitigating systems cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage).

The inspectors reviewed IMC 0609, Significance Determination Process, Appendix A, Determining the Significance of Reactor Inspection Findings for At-Power Situations, dated March 23, 2007, and determined that since the finding affected fire protection, a significance determination evaluation under IMC 0609, Appendix F, was required. The inspectors completed a significance determination of this issue using IMC 0609, Appendix F, Fire Protection Significance Determination Process, dated February 28, 2005. This finding screened to a Phase 2 analysis in accordance with SDP Phase 1 using Attachment 2, Degradation Rating Guidance Specific to Various Fire Protection Program Elements. The inspectors assigned a degradation rating of moderate because of procedural inconsistencies between BOP FR-1 and the Fire Safe Shutdown analysis.

The inspectors and the SRA performed a SDP evaluation to determine the risk-significance of this finding. The inspectors determined that the finding potentially affected the ability of the charging pumps to perform their safe shutdown function.

The spurious opening of either valve SI 8811A or SI 8811B combined with the inadequate procedural guidance for operators to mitigate this spurious actuation would result in draining the RWST inventory to the containment sump. During a fire event, the operating charging pump suction would be aligned to the RWST and would therefore be vulnerable to failure from loss of suction if the RWST contents drain to the containment sump. The inspectors determined that the procedural guidance was inadequate for a fire in the AEER and in the main control room. As a result the SDP considered fire scenarios in these two plant areas.

For a fire in the AEER, the inspectors and the SRA completed a Phase 2 SDP evaluation using IMC 0609, Appendix F, Fire Protection SDP. Based on information provided by the licensee, the inspectors determined that the spurious operation of SI8811A or SI8811B could occur if a fire affected either cabinet PA09J or PA10J in the AEER. The inspectors further determined that a fire in either of these panels was unlikely to spread within the AEER to affect a second division of safe shutdown equipment due to lack of intervening combustibles and the distance between the divisions within the room. Furthermore, a credible fire in either of these panels would not result in a loss of offsite power, or a small loss of coolant accident due to an inadvertant opening of the power operated relief valve (PORV). Therefore, the Phase 2 analysis considered a fire in either cabinet PA09J or PA10J that could induce a spurious opening of either SI8811A or B, which would result in the loss of one train of safe shutdown equipment. From Appendix F Step 2.4, the fire frequency for a single cabinet is 6.0E-5/yr. Since the two cabinets contributed to this finding, the frequency of the fire is 1.2E-4/yr. Also from Appendix F, Step 2.5, one division of equipment remained available for safe shutdown and was credited with a failure probability of 1.0E-2/yr.

Finally, from Step 2.8 of Appendix F, the probability of a spurious opening of the valve was estimated at 0.6. The final result of the change in risk for the AEER fire was estimated at 7.2E-7/yr.

For a fire in the control room, the SRA completed a Phase 3 SDP evaluation using information from IMC 0609, Appendix F, and from the licensees Individual Plant Examination for External Events (IPEEE) submittal. Based on information provided by the licensee and a walkdown of the control room, a fire in the main control room panel PM06J(A2) would be necessary to cause the spurious opening of SI 8811A or B. From the IPEEE, the SRA determined that a fire in this panel could affect auxiliary feedwater (AFW) pump 1B, both trains of safety injection (SI), both trains of RHR, manual reactor trip, manual safety injection switch, manual main steam isolation switch, manual Phase A isolation, and manual containment spray actuation switch. The SRA determined that offsite power, PORVs, and charging would not be affected by a fire contained in this cabinet. However, because of the inadequate procedure that could result in draining the RWST to the containment sump if the spurious valve opening occurred, the charging pumps could now also be affected due to loss of suction.

To estimate the fire frequency, the SRA used the main control board frequency from Appendix F (4.8E-3) and divided it by the number of control room cabinets listed in the licensees IPEEE (31). The result was a fire frequency of 1.5E-4/yr for a single cabinet.

No suppression of the fire prior to damage within the cabinet was evaluated. It was assumed that the fire would fail all of the functions listed above and would cause the spurious opening of the valve causing the draining of the RWST. To estimate a conditional core damage probability, the SRA used the Simplified Plant Analysis Risk Model, version 3.21 for Byron. The initiating event was assumed to be a transient with the loss of the power conversion system. The base case conditional core damage probability was estimated assuming AFW pump 1B, both SI trains, and both RHR trains were failed. The AFW pump was assumed to be recoverable since it is a diesel-driven pump that can be started and run locally. The current case to evaluate the delta risk due to the deficient procedure assumed that the charging pumps would fail with a failure probability of 0.6, to represent the probability of a spurious opening of the valve. No other spurious actuations were assumed to occur. The overall delta core damage frequency estimate given these assumptions for the control room fire was 2.1E-7/yr.

This analysis did not consider the control room evacuation scenario but assumed that the frequency of such a fire event would be less than the fire scenario considered here.

The total delta risk for both fire scenarios was 9.3E-7/yr which represented a finding of very low safety significance (Green). The result was bounding given that there was no credit for fire suppression prior to damage and no credit for operator manual actions to control equipment in the plant. The dominant sequence involved a fire in either the AEER or main control room that resulted in the spurious opening of SI 8811A or B, random failure of AFW, and failure of feed and bleed.

Enforcement:

License condition 2.C.6 and 2E of the Byron Station Operating License for Unit 1 and 2 respectively required, in part, that the licensee implement and maintain in effect all provisions of the approved fire protection program as described in the licensees Fire Protection Report, and as approved in the Safety Evaluation Report dated February 1987 through Supplement No. 8. Section 3.5.c Alternative or Dedicated Shutdown Capability, Paragraph (3) [10 CFR Part 50, Appendix R,Section III.L.3] of the FPR in response to Appendix A of BTP [Branch Technical Position] APCSB 9.5-1 stated, that the shutdown capability for specific fire areas may be unique for each such area, or it may be one unique combination of systems for all such areas. In either case, the alternative shutdown capability shall be independent of the specific fire area(s). In addition, procedures shall be in effect to implement the alternative shutdown capability. This section of the FPR also indicated the licensees response stated that the station complied with this NRC guideline.

Contrary to the above, in June 2004, the inspectors identified that Procedure BOP FR-1 Fire Response Guidelines, Revision 6, was not adequate to implement the alternative shutdown capability. Specifically, Attachments 35 and 38 of Procedure BOP FR-1 for a fire in the auxiliary electrical equipment room and control room respectively, did not provide adequate instructions to prevent the draining of the RWST and did not direct the operators to use cold leg injection in the event that the RWST drained to the containment sump. Once identified, the licensee entered the issue into the corrective action program under AR 00234512 and revised Procedure BOP FR-1, by adding steps earlier in the procedure to promptly assure an adequate RWST inventory was maintained. Because this violation was of very low safety significance and it was entered into the licensees corrective action program, this violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy.

(NCV 05000454/2007002-02; 05000455/2007002-02)

1R06 Flood Protection Measures

1. Internal Flooding Review

a. Inspection Scope

The inspectors evaluated the internal flooding controls for the following areas:

This review represented one inspection sample. Documents reviewed during this inspection are listed in the Attachment to this report.

b. Findings

On March 14, 2007, the inspectors entered the Unit 1 Auxiliary Feedwater (AFW)

Tunnel as part of this inspection. The licensee had opened two of the four bolted down flood seal hatches for the tunnel for routine work activities. The inspectors observed that flood seal 1DSFS007 had some of its gasket missing. The flood seal looked normal from above but when viewed from below approximately three feet of gasket material were hanging down into the tunnel. The licensee initiated an IR and repaired the gasket while the other flood seals were still open.

On March 19, the inspectors performed a routine verification that the Unit 1 AFW tunnel hatches had been properly re-installed. The inspectors determined that hatch 1DSFS008 had not been properly re-installed. The hatch was bent upwards along one corner resulting in a narrow opening of approximately seven square inches. The inspectors questioned licensee personnel regarding the as-found condition of the hatch.

The licensee initiated IR 605830, which stated that the flood seals were still able to protect the AFW isolation valves and that the AFW isolation valves could still perform their containment isolation function.

The inspectors questioned the licensees basis for operability. Licensee personnel were unable to provide an adequate bases for operability of the AFW isolation valves.

Licensee personnel immediately restored the AFW tunnel hatch/flood seal to the as-designed configuration and began performing a more detailed operability assessment. By the end of the report period the detailed operability assessment was not complete. Pending receipt from the licensee and the inspectors review of the detailed operability assessment the past operability of the safety related equipment in the AFW tunnel will remain an Unresolved Item (URI)05000454/2007002-03.

1R07 Heat Sink Performance

.1 Biennial Review of Heat Sink Performance

a. Inspection Scope

The inspectors reviewed the performance of the Unit 2 Train A SX pump lube oil cooler and the Unit 2 Train B Diesel-Driven AFW pump closed cycle cooler. These heat exchangers were chosen for review based on many factors, e.g., their high risk-assessment worth in the licensees probabilistic safety analysis, their important safety-related mitigating system support functions, and relatively low margin. This review resulted in the completion of two inspection samples. While on-site, the inspectors verified that the licensees inspection, engineering and maintenance activities were adequate to ensure proper heat transfer. This was done by reviewing the methods used to inspect and test the heat exchangers, verifying that the as-found inspection results were appropriately dispositioned, and interviewing personnel. The inspectors also verified, by review of procedures, test results, and interviews that chemical treatments, ultrasonic tests, and methods used to control biotic fouling, corrosion and macro-fouling were sufficient to ensure required heat exchanger performance.

The inspectors verified that the condition and operation of these heat exchangers were consistent with design assumptions in heat transfer calculations by reviewing related calculations, inspect/clean work orders, procedures and completed surveillance tests.

Also while on-site, the inspectors verified three attributes of the ultimate heat sink (UHS)as required by IP 71111.07B, Section 2.02, items d.1, d.2, and d.7.

The inspectors verified proper maintenance of inaccessible below-water portions of the UHS system by reviewing the methodology and results of underwater diving inspection documentation which demonstrated UHS capability. The licensees underwater inspection ensured UHS capacity by monitoring and removing sediment intrusion as necessary and ensuring structural integrity of underwater UHS structures, weirs, and excavations by any necessary inspection and repairs. The inspectors reviewed associated calculations to ensure UHS capacity would support safety function performance. The inspectors also confirmed that the calculation and inspection methodologies were consistent with accepted NRC and industry practices.

The inspectors reviewed corrective action documents, concerning heat exchanger or heat sink performance issues to verify that the licensee had an appropriate threshold for identifying issues. The inspectors also evaluated the effectiveness of the corrective actions for identified issues, including the engineering justifications for operability.

Documents reviewed during this inspection are listed in the Attachment to this report.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification

.1 Resident Inspector Quarterly Review

a. Inspection Scope

The inspectors completed one inspection sample by observing and evaluating an operating crew during a reactor trip and anticipated transient without scram with failure of Unit 1 Loop A Steam Generator Power Operated Relief Valve. The inspectors evaluated crew performance in the areas of:

  • Clarity and formality of communications;
  • Ability to take timely actions;
  • Prioritization, interpretation, and verification of alarms;
  • Procedure use;
  • Control board manipulations;
  • Supervisors command and control;
  • Management oversight; and
  • Group dynamics.

The inspectors verified that the crew completed the critical tasks listed in the above simulator guide. The inspectors also compared simulator configurations with actual control board configurations. For any weaknesses identified, the inspectors observed the licensee evaluators to determine whether they also noted the issues and discussed them in the critique at the end of the session. The inspectors verified that minor issues were placed into the licensees corrective action program.

The documents reviewed during this inspection are listed in the Attachment to this report.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors completed one inspection samples by evaluating the licensees implementation of the maintenance rule, 10 CFR 50.65, as it pertained to identified performance problems associated with the following structures, systems, and/or components:

  • Unit 1 and 2 Rod Control Circuit Cards Failure.

The inspectors evaluated the licensee's appropriate handling of structures, systems, and components (SSC) condition problems in terms of appropriate work practices and characterizing reliability issues. Equipment problems were screened for review using a problem oriented approach. Work practices related to the reliability of equipment maintenance were observed during the inspection period. Items chosen were risk significant, and extent of condition was reviewed as applicable. Work practices were reviewed for contribution to potential degraded conditions of the affected SSCs. Related work activities were observed and corrective actions were discussed with licensee personnel. The licensee's handling of the issues being reviewed was evaluated under the requirements of the maintenance rule.

The inspectors also reviewed selected issues documented in IRs, to determine if they had been properly addressed in the licensees corrective action program. The documents reviewed during this inspection are listed in the Attachment to this report.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed the licensees management of plant risk during emergent maintenance activities or during activities where more than one significant system or train was unavailable. The inspectors chose activities based on their potential to increase the probability of an initiating event or impact the operation of safety-significant equipment. The inspectors verified that the evaluation, planning, control, and performance of the work were done in a manner to reduce the risk and the work duration was minimized where practical. The inspectors also verified that contingency plans were in place where appropriate.

The inspectors reviewed configuration risk assessment records, UFSAR, TS, and Individual Plant Examination. The inspectors also observed operator turnovers, observed plan-of-the-day meetings, and reviewed other related documents to determine that the equipment configurations had been properly listed, that protected equipment had been identified and was being controlled where appropriate, and that significant aspects of plant risk were being communicated to the necessary personnel.

The inspectors completed seven inspection samples by reviewing the following activities:

  • Unit 2 Train A Solid State Protection System Testing while Unit 2 Train A Residual Heat Removal Pump was out of service (OOS);
  • Unit 2 Rod Control Emergent Failure while DC Bus 112 was Cross-tied to DC Bus 212;
  • Unit 2 Train B Essential Service Water Pump Work Window while "D" Reactor Containment Fan Cooler was OOS;
  • Emergent Work for Unit 0 Train B Non-Essential Service Water Pump High Bearing Temperature; and
  • Unit 2 Unexpected Letdown Isolation and Resultant Unrecognized Entry into a Yellow On-Line Risk Configuration.

The documents reviewed during this inspection are listed in the Attachment to this report.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations

a. Inspection Scope

The inspectors evaluated plant conditions, selected condition reports, engineering evaluations, and operability determinations for risk-significant components and systems in which operability issues were questioned. These conditions were evaluated to determine whether the operability of components was justified.

The inspectors completed seven samples by reviewing the following evaluations and issues:

  • Plugged Fire Nozzles in Unit 2 Train B Diesel Generator Fuel Oil Storage Tank Room;
  • Unit 0 Train A Essential Service Water Makeup Pump Fuel Oil Contamination;
  • Non Safety Related Filters Installed in Safety Related Ventilation Systems;
  • Flood Seal and High Energy Line Break Barrier Hatches to the AFW Tunnel Not Properly Secured; and
  • Different Material Used in Essential Service Water Fan Blade Clamps.

The inspectors compared the operability and design criteria in the appropriate section of the TS including the TS Basis, the Technical Requirements Manual (TRM) and UFSAR to the licensees evaluations to determine that the components or systems were operable. The inspectors determined whether compensatory measures, if needed, were taken, and determined whether the evaluations were consistent with the requirements of licensee procedures. The inspectors also discussed the details of the evaluations with the shift managers and appropriate members of the licensees engineering staff.

The inspectors also reviewed selected issues documented in IRs, to determine if they had been properly addressed in the licensees corrective action program. The documents reviewed during this inspection are listed in the Attachment to this report.

b. Findings

No findings of significance were identified.

1R19 Post Maintenance Testing

a. Inspection Scope

The inspectors reviewed the post maintenance testing activities associated with maintenance or modification of mitigating, barrier integrity, and support systems that were identified as risk significant in the licensees risk analysis. The inspectors reviewed these activities to determine that the post maintenance testing was performed adequately, demonstrated that the maintenance was successful, and that operability was restored. During this inspection activity, the inspectors interviewed maintenance and engineering department personnel and reviewed the completed post maintenance testing documentation. The inspectors used the appropriate sections of the TS, TRM, and UFSAR, and other related documents to evaluate this area.

The inspectors completed four inspection samples by observing and evaluating the post maintenance testing subsequent to the following maintenance activities:

  • Unit 2 Train B Safety Injection Pump Work Window;
  • Unit 1 Train A Diesel Generator Lubricating Oil Pump Following Maintenance;
  • Unit 2 Division 22 Direct Current Bus Work Window; and
  • Unit 0 Train A Essential Service Water Basin Level Switch Replacement.

The inspectors also reviewed selected issues documented in IRs to determine if they had been properly addressed in the licensees corrective action program. The documents reviewed during this inspection are listed in the Attachment to this report.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors witnessed selected surveillance tests and/or reviewed test data to determine that the equipment tested using the surveillance procedures met the TS, the TRM, the UFSAR and licensee procedural requirements. The inspectors also reviewed applicable design documents including plant drawings, to verify that the surveillance tests demonstrated that the equipment was capable of performing its intended safety functions. The activities were selected based on their importance in ensuring mitigating systems capability and barrier integrity.

These activities represented seven routine samples. The following surveillance tests were selected:

  • Unit 2 Train A Safety Injection Pump Group A Inservice Test;
  • Unit 2 Engineered Safety Features Activation System Instrument Slave Relay Surveillance (Train B Automatic Containment Spray Relay K644);
  • Unit 2 Train A Solid State Protection System Bi-Monthly Surveillance; and

Additionally the inspectors used the documents listed in the Attachment to this report to determine that the testing met the frequency requirements; that the tests were conducted in accordance with procedures, that the test acceptance criteria were met; and that the results of the tests were properly reviewed and recorded. The inspectors verified that the individuals performing the tests were qualified to perform the test in accordance with the licensees requirements, and that the test equipment used during the test were calibrated within the specified periodicity. In addition, the inspectors interviewed operations, maintenance, and engineering department personnel regarding the tests and test results.

The documents reviewed during this inspection are listed in the Attachment to this report.

b. Findings

No findings of significance were identified.

1R23 Temporary Plant Modifications

a. Inspection Scope

The inspectors completed one inspection sample by evaluating the following temporary plant modification on risk significant equipment:

  • Bypass of General Warning Relay K524 Contact 6-10 During Train A Solid State Protection System Surveillance The inspectors reviewed this temporary plant modification to determine that the instructions were consistent with applicable design modification documents and that the modification did not adversely impact system operability or availability. The inspectors verified that the licensee controlled temporary modifications in accordance with Nuclear Station Procedure NSP CC-AA-112, Temporary Configuration Changes, Revision 11.

The documents reviewed during this inspection are listed in the Attachment to this report.

b. Findings

No findings of significance were identified.

RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS1 Access Control to Radiologically Significant Areas (71121.01)

.1 Inspection Planning

a. Inspection Scope

The inspectors reviewed all licensee Performance Indicators (PIs) for the Occupational Exposure Cornerstone for followup. This review represented one sample.

b. Findings

No findings of significance were identified.

.2 Plant Walkdowns and Radiation Work Permit (RWP) Reviews

a. Inspection Scope

The inspectors identified exposure significant work areas within radiation areas, high radiation areas (HRA) (<1 R/hr), and airborne radioactivity areas in the plant and reviewed associated licensee controls and surveys of these areas to determine if controls (e.g., surveys, postings, barricades) were acceptable.

The inspectors walked down these areas or their perimeters with a survey instrument to identify whether prescribed RWP(s), procedure(s), and engineering controls were in place, whether licensee surveys and postings were complete and accurate, and whether air samplers were properly located.

The inspectors reviewed RWPs used to access these and other HRA to identify what work control instructions or control barriers were specified using plant-specific TS HRA requirements as the standard for the necessary barriers. The inspectors reviewed electronic personal dosimeter (EPD) alarm set points (both integrated dose and dose rate) for conformity with survey indications and plant policy. The inspectors verified that workers knew what actions were required when their EPD noticeably malfunctions or alarms.

The inspectors reviewed RWPs for airborne radioactivity areas with the potential for individual worker internal exposures of >50 mrem committed effective dose equivalent (CEDE) (20 DAC-hrs). No areas of the plant were under airborne radioactivity work controls.

The inspectors reviewed the adequacy of the licensees internal dose assessment for any actual internal exposure greater than 50 mrem CEDE. No personnel had documented committed effective dose equivalent greater than 50 millirem.

The inspectors examined the licensees physical and programmatic controls for highly activated or contaminated materials (non-fuel) stored within spent fuel and other storage pools.

These reviews represented six samples.

b. Findings

No findings of significance were identified.

.3 Problem Identification and Resolution

a. Inspection Scope

The inspectors reviewed the licensees self-assessments, audits, Licensee Event Reports, and Special Reports related to the access control program since the last inspection. The inspectors assessed whether identified problems were entered into the corrective action program for resolution.

The inspectors reviewed corrective action reports related to access controls. Included in this review were HRA, radiological incidents (non-PIs, identified by the licensee) in HRAs <1R/hr that have occurred since the last inspection in this area. The inspectors interviewed staff and reviewed documents to assess if the follow-up activities were being conducted in an effective and timely manner commensurate with their importance to safety and risk:

  • Initial problem identification, characterization, and tracking;
  • Disposition of operability/reportability issues;
  • Evaluation of safety significance/risk and priority for resolution;
  • Identification of repetitive problems;
  • Identification of contributing causes;
  • Identification and implementation of effective corrective actions;
  • Resolution of Non-Cited Violations (NCVs) tracked in the corrective action system; and
  • Implementation/consideration of risk significant operational experience feedback.

The inspectors review placed emphasis on ensuring problems were identified, characterized, prioritized, entered into a corrective action, and resolved.

The inspectors assessed if the licensees self-assessment activities are also identifying and addressing repetitive deficiencies or significant individual deficiencies in problem identification and resolution.

These reviews represented three samples.

b. Findings

No findings of significance were identified.

.4 High Risk Significant, High Dose Rate HRA (>25 rem in one hour at 30 cm), and

VHRA Controls

a. Inspection Scope

The inspectors discussed with first-line health physics supervisors, or equivalent positions, having back shift health physics oversight authority, the controls in place for special areas that have the potential to become VHRA during certain plant operations.

The inspectors reviewed how the required communications between the health physics group and other involved groups would occur beforehand in order to allow corresponding timely actions to properly post and control the radiation hazards.

The inspectors verified adequate posting and locking of all entrances to all accessible high dose rate HRAs (>25 rem in one hour at 30 cm) and VHRA.

These reviews represented two samples.

b. Findings

No findings of significance were identified.

2OS2 As-Low-As-Is-Reasonably-Achievable Planning and Controls (ALARA) (71121.02)

.1 Verification of Dose Estimates and Exposure Tracking Systems

a. Inspection Scope

The inspectors reviewed the assumptions and basis for the current annual collective exposure estimate. The inspectors reviewed applicable procedures to determine the methodology for estimating work activity-specific exposures and the intended dose outcome. The inspectors evaluated both dose rate and man-hour estimates for reasonable accuracy.

The inspectors reviewed the licensees method for adjusting exposure estimates or re-planning work, when unexpected changes in scope or emergent work are encountered.

These reviews represented two samples.

b. Findings

No findings of significance were identified.

.2 Problem Identification and Resolution

a. Inspection Scope

The inspectors reviewed the licensees self-assessments, audits, and Special Reports related to the ALARA program since the last inspection. The inspectors review was conducted to determine if the licensees overall audit programs scope and frequency (for all applicable areas under the Occupational Cornerstone) satisfied the requirements of 10 CFR 20.1101(c).

These reviews represented two samples.

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES

4OA2 Identification and Resolution of Problems

.1 Review of Items Entered into the Corrective Action Program:

a. Inspection Scope

As required by Inspection Procedure 71152, Identification and Resolution of Problems, and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed screening of all items entered into the licensees corrective action program. This was accomplished by reviewing the description of each new Issue Report and attending selected daily management review committee meetings. Documents reviewed are listed in the Attachment to this report.

b. Findings

No findings of significance were identified.

.2 Selected Issue Follow-up Review - Recurring Issue Review

a. Introduction During this quarter, the inspection identified three minor issues that were related to inadequate control of lubricating oil level setting, inadequate risk management action and inadequate seismic control of cryogenic liquid nitrogen containers. These issue had been identified within the past year and involved different areas of licensee operations.

b. Prioritization and Evaluation of Issue

(1) Inspection Scope The inspectors reviewed the cause evaluation of the past events and compared the evaluation method used to the guidance provided in licensees procedures. The inspectors also compared the present events with the past events and discussed the technical aspects of the issues with members of the licensees staff.
(2) Issues Inadequate Control of Lubricating Oil Level Setting: On February 22, 2007, during a routine system alignment walkdown, the inspectors identified that the Unit 2 Train A Essential Service Water pump motor oil level were all above the highest unlabeled mark on the sight glass. The inspectors informed plant operations and reviewed a subsequent operability assessment. The assessment stated that this condition was acceptable because the mark was unlabeled and there had not been a bearing failure in 20 years of operation.

The inspectors reviewed the motor vendor manual and the nameplate data on the side of the motor and determined that the vendor recommendation was to set the level with the motor not running and to maintain the level below the highest mark on the sight glass. When asked by the inspectors, licensee personnel were not aware of the vendor recommendation. The licensee subsequently lowered the level of the oil in the constant level oilers to the recommended level. Note that the SX motor bearing oil system is an example of a constant level oiler. The enforcement aspect of this finding was provided in Section 1R04 of this report.

On November 17, 2006, the inspectors also identified a finding of very low safety significance (Green) related to the licensees failure to maintain setpoint control of Trico constant level oilers. The oilers are used on the five safety related Component Cooling Water pumps. This condition increased the challenges to the proper functioning of the lubricating oil and thus to the bearings of the safety related pumps. Corrective actions at that time focused on the new corporate level procedure for setting constant level oilers, which primarily focused on Trico oilers that were used on the CCW pumps, and ensuring the Trico oilers were installed on the correct side of the bearing housing. The extent of condition review failed to consider other manufacturers of constant level oilers.

Inadequate risk management action: On March 8, 2007, during the performance of the Unit 2 Train B Essential Service Water oil cooler inspection, the inspectors identified that a protected equipment barrier for the Unit 2 Train A Essential Service Water pump was not installed in front of the room door in accordance with Operation Policy 400-47. The omission was determined to be a human error on creating the list of protected equipment. The inspector determined that this issue was a violation of 10CFR50.65(a)4 because one or more risk management actions were not effectively implemented. This issue was determined to be minor because all key safety functions were preserved and the increase in plant risk was less than or equal to the industry guidance threshold for taking risk management actions. Corrective action included a revision to the operating policy to add a peer check to prevent errors.

During the 4th quarter of 2006, the inspectors also identified that the Unit 2 Train A Residual Heat Removal pump cubical cooler breaker was not protected as required by procedure. At that time, licensee staff stated they were confused about what constituted the extent of the protected equipment boundary. This issue was determined to be minor as it was less than or equal to the industry guidance threshold for taking risk management actions. Corrective action included revising the operation policy to provide clarification and direction on protected equipment boundary. This revision has yet to be completed.

Inadequate Seismic Control of Cryogenic Liquid Nitrogen Containers: On March 14, 2007, the inspectors identified that cryogenic liquid storage (nitrogen)containers were not properly secured in the auxiliary building. The inspectors contacted a mechanical maintenance supervisor and were told that these containers did not need to be secured. However, when a senior reactor operator was contacted later, he stated that containers needed to be secured. The inspector determined that the requirements for seismic control of the cryogenic liquid nitrogen containers were not well understood by plant personnel. The licensee later changed the work package to secure the containers at the job site.

In the first quarter of 2006, the inspectors also identified that several cryogenic liquid nitrogen containers were not secured in the auxiliary building. Corrective action at the time included a discussion at the weekly safety meeting for mechanical maintenance personnel to reinforce the expectation and procedure requirement. However, based on the recurrence of the problem, these corrective actions were not effective.

c. Effectiveness of Correction Actions

(1) Inspection Scope The inspectors assessed the licensees corrective actions associated with the three past events and the three current events to determine if the corrective actions were appropriately focused to address the problems identified.
(2) Issues The inspectors reviewed the licensees correction actions associated with the three past events and determined that the corrective actions were appropriate and addressed the causes identified. However, the extent of condition reviews were narrowly focused. In the case of the oilers, the licensee also initiated a comprehensive review of the Trico oilers used in the plant but the review did not extend to other types of constant oiler. In the case of the protected equipment barrier not being installed, the licensee did not establish a verification check that could identify errors in the list of protected equipment.

In the case of the unsecured cryogenic containers, the licensee did not periodically communicate or provide adequate training to its staff to make clear the seismic control requirements.

In summary, these three issues were minor in nature and corrective actions to prevent reoccurrence were not required by NRC regulations. Nevertheless, the licensee was taking actions to correct the weaknesses in these areas.

c. Findings

No findings of significance were identified.

4OA5 Other Activities

.1 (Closed) Unresolved Item (URI)05000454/2004005-03; 05000455/2004005-03:

Adequacy of Safe Shutdown Procedure to Address Draining of the RWST An URI was opened during the 2004 Triennial Fire Protection Inspection regarding the adequacy of alternate safe shutdown procedures in the event of a fire in the auxiliary electrical equipment room or the control room. Based on the information discussed in Section 1R05.b.1 of this report, an NCV of the Byron Station Operating License 2.C.6 (Unit 1) and 2.E (Unit 2) was identified. Therefore, this URI is closed.

.2 (Closed) Unresolved Item 05000454/2006004-04; 05000455/20060004-04: Impact of

Nonfunctional Dosimeters on Dose Tracking and Technical Specification Compliance During a baseline radiation safety inspection, inspectors identified abnormal radiological restricted area exit electronic dosimetry transaction records related to a condition identified as Electronic Dosimetry Digi Reset. The Digi Reset condition represented an event when the dosimeter appeared to be non-functioning for a period of time ranging up to 15 minutes. Consequently, it appeared that the electronic dosimeter would not continuously integrate the radiation dose rate in the area and would not alarm when a preset integrated dose was received. The inspectors reviewed the technical cause for this condition, actions taken by the manufacturer, and the radiological impact of the condition. The licensees technical evaluation demonstrated that the reset event was a very short lived event (fractions of a second). However, the dose integration function was affected by data archival durations set in the software code. The licensee performed additional investigations to determine the specific instances when the Digi-Reset problem occurred, quantifying the duration that the dosimeter was not functioning and the amount of dose that was not integrated, and completed its evaluation for compliance with the requirements specified in TS 5.7 Administrative Controls for High Radiation Areas. From the licensees data, the inspectors observed that the very brief interruptions were well within the expected operation of the instrumentation and did not represent any violations of NRC requirements.

Consequently, the inspectors concluded that the short duration of the power interruption and the minimal amount of dose that might not be integrated does not represent an occurrence in the Occupational Radiation Safety PI as defined in the Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline.

Therefore, this URI is closed.

4OA6 Meetings

.1 On April 06, 2007, the resident inspectors presented the inspection results to

Mr. D. Hoots and his staff, who acknowledged the findings. The inspectors asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.

.2 Interim Exit Meetings

Interim exits were conducted for:

  • Heat Sink Biennial Inspection with Mr. D. Hoots and other members of licensee management on February 9, 2007.
  • Occupational Radiation Safety Program for Access Control to Radiologically Significant Areas and As-Low-As-Reasonably-Achievable (ALARA) Planning and Controls programs with Ms. M. Snow on February 16, 2007.

4OA7 Licensee Identified Violations

The following violation of very low safety significance (Green) was identified by the licensee and is a violation of NRC requirements which meet the criteria of Section VI of the NRC Enforcement Manual, NUREG-1600, for being dispositioned as an NCV.

Cornerstone: Mitigating Systems

Technical Specification 5.4 required implementation of the applicable procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A. Regulatory Guide 1.33, Appendix A, Part 9, Subsection e, recommended procedures for the control of maintenance and factors to be taken into account in preparing work procedures. Contrary to this requirement, the licensee failed to implement the procedure for the on-line work control process. Specifically, corporate Procedure WC-AA-101, Revision 13, On -Line Work Control Process, Step 4.1.1, states, in part, Risk shall be reassessed if emergent condition results in a plant configuration that has not been previously assessed. [Original emphasis retained.]

Contrary to the above, on February 24, 2007, the licensee failed to reassess risk following the emergent condition requiring that both Unit 2 regenerative heat exchangers be removed from service due to letdown flow issues. This condition rendered pressurizer auxiliary spray as not available. With pressurizer auxiliary spray not available on-line risk changed from a Green to a Yellow Condition. The licensee recognized the missed risk assessment on February 26, 2007, and to the appropriate actions in accordance with their risk control process. This issue was considered to be of very low safety significance because the change in core damage frequence was less than 10 E -12. This issue was entered into the licensees corrective action system as IR 596192.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

D. Hoots, Site Vice President
M. Snow, Plant Manager
B. Barton, Radiation Engineering Superintendent
F. Beutler, Engineering, Fire Protection
D. Bohnert, UHS System Engineer
D. Combs, Security Manager
L. Doyle, Programs Coordinator
A. Giancatarino, Engineering Director
C. Gregory, RP Instrumentation Coordinator
W. Grundmann, Regulatory Assurance Coordinator
T. Hulbert, Regulatory Assurance
J. Langan, Regulatory Assurance
V. Naschansky, Supervisor, Design Engineering, Electrical
S. Swanson, Maintenance Director
D. Palmer, Radiation Protection Manager,
W. Kouba, Nuclear Oversight Manager
M. Prospero, Operations Manager
J. Roman, IEMA, Springfield
D. Sargent, Mechanical Design Engineer
D. Thompson, Technical Support Superintendent
N. Vakili, GL 89-13 Program Owner, Program Engineer

Illinois Emergency Management Agency

R. Zuffa, Section Supervisor, Resident Inspector

Nuclear Regulatory Commission

S. West, Deputy Director, Division of Reactor Projects
R. Skokowski, Chief, Branch 3, Division of Reactor Projects
D. Passehl, Senior Risk Analyst, Division of Reactor Safety
P. LaFlamme, Reactor Engineer, Inspector in Training Branch 3
L. Kozak, Senior Risk Analyst, Division of Reactor Safety

Attachment

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000455/2007002-03 URI Operability of the Flood Seals to the Unit 1 AFW Tunnel with One Corner Raised Up

Opened and Closed

05000454/2007002-01 FIN Inadequate Setpoint Control of the Oil Level to Safety
05000455/2007002-01 Related Pumps
05000454/2007002-02 NCV Adequacy of Safe Shutdown Procedures to Address
05000455/2007002-02 Draining of the RWST

Closed

05000454/2004005-03 URI Adequacy of Safe Shutdown Procedures to Address
05000455/2004005-03 Draining of the RWST
05000454/2006004-04; URI Impact of Nonfunctional Dosimeters on Dose Tracking
05000455/2006004-04 and TS Compliance

Discussed

None Attachment

LIST OF DOCUMENTS REVIEWED