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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217M4461999-10-20020 October 1999 Forwards Rev 8 to Sequoyah Nuclear Plant Physical Security/ Contingency Plan, IAW 10CFR50.54(p).Encl Withheld,Per 10CFR73.21 ML20217J4151999-10-15015 October 1999 Forwards Request for Addl Info Re Util 990624 Application for Amend of TSs That Would Revise TS for Weighing of Ice Condenser Ice Baskets 05000327/LER-1999-002, Forwards LER 99-002-00 Re Start of Units 1 & 2 EDGs as Result of Cable Being Damaged During Installation of Thermo- Lag for Kaowool Upgrade Project1999-10-15015 October 1999 Forwards LER 99-002-00 Re Start of Units 1 & 2 EDGs as Result of Cable Being Damaged During Installation of Thermo- Lag for Kaowool Upgrade Project ML20217G1141999-10-0707 October 1999 Responds to from P Salas,Providing Response to NRC Risk Determination Associated with 990630 Flooding Event at Sequoyah Facility.Meeting to Discuss Risk Determination Issues Scheduled for 991021 in Atlanta,Ga ML20217B2981999-10-0606 October 1999 Discusses Closeout of GL 92-01,rev 1,suppl 1, Reactor Vessel Integrity, for Sequoyah Nuclear Plant,Units 1 & 2. NRC Also Hereby Solicits Any Written Comments That TVA May Have on Current Rvid Data by 991101 ML20217B8431999-10-0505 October 1999 Requests NRC Review & Approval of ASME Code Relief Requests That Were Identified in Plant Second 10-yr ISI Interval for Both Units.Encl 3 Provides Util Procedure for Calculation of ASME Code Coverage for Section XI Nondestructive Exams IR 05000327/19990041999-10-0101 October 1999 Ack Receipt of Providing Comments on Insp Repts 50-327/99-04 & 50-328/99-04.NRC Considered Comments for Apparent Violation Involving 10CFR50.59 Issue ML20217C7101999-10-0101 October 1999 Forwards Response to NRC 990910 RAI Re Sequoyah Nuclear Plant,Units 1 & 2 URI 50-327/98-04-02 & 50-328/98-04-02 Re Ice Weight Representative Sample ML20212J5981999-10-0101 October 1999 Forwards SE Accepting Request for Relief from ASME Boiler & Pressure Vessel Code,Section Xi,Requirements for Certain Inservice Insp at Plnat,Unit 1 ML20212M1081999-09-29029 September 1999 Confirms Intent to Meet with Utils on 991025 in Atlanta,Ga to Discuss Pilot Plants,Shearon Harris & Sequoyah Any Observations & Lessons Learned & Recommendations Re Implementation of Pilot Program ML20217A9451999-09-27027 September 1999 Forwards Insp Repts 50-327/99-05 & 50-328/99-05 on 990718- 0828.One Violation Identified & Being Treated as Non-Cited Violation ML20216J9351999-09-27027 September 1999 Responds to NRC Re Violations Noted in Insp Repts 50-327/99-04 & 50-328/99-04.Corrective Actions:Risk Determination Evaluation Was Performed & Licensee Concluded That Event Is in Green Regulatory Response Band ML20212F0751999-09-23023 September 1999 Forwards SER Granting Util 981021 Request for Relief from ASME Code,Section XI Requirements from Certain Inservice Insp at Sequoyah Nuclear Power Plant,Units 1 & 2 Pursuant to 10CFR50.55a(a)(3)(ii) ML20212F4501999-09-23023 September 1999 Forwards Amends 246 & 237 to Licenses DPR-77 & DPR-79, Respectively & Ser.Amends Approve Request to Revise TSs to Allow Use of Fully Qualified & Tested Spare Inverter in Place of Any of Eight Required Inverters ML20212M1911999-09-21021 September 1999 Discusses Exercise of Enforcement Discretion Re Apparent Violation Noted in Insp Repts 50-327/99-04 & 50-328/99-04 Associated with Implementation of Procedural Changes Which Resulted in Three Containment Penetrations Being Left Open ML20211Q0311999-09-10010 September 1999 Requests Written Documentation from TVA to Provide Technical Assistance to Region II Re TS Compliance & Ice Condenser Maint Practices at Plant ML20216F5441999-09-0707 September 1999 Provides Results of Risk Evaluation of 990630,flooding Event at Sequoyah 1 & 2 Reactor Facilities.Event Was Documented in Insp Rept 50-327/99-04 & 50-328/99-04 & Transmitted in Ltr, ML20211N5681999-09-0101 September 1999 Submits Clarification of Two Issues Raised in Insp Repts 50-327/99-04 & 50-328/99-04,dtd 990813,which Was First Insp Rept Issued for Plant Under NRC Power Reactor Oversight Process Pilot Plant Study ML20211G5881999-08-27027 August 1999 Submits Summary of 990820 Management Meeting Re Plant Performance.List of Attendees & Matl Used in Presentation Enclosed ML20211F8891999-08-25025 August 1999 Forwards Sequoyah Nuclear Plant Unit 1 Cycle 9 Refueling Outage, Re Completed SG Activities,Per TSs 4.4.5.5.b & 4.4.5.5.c ML20211A1851999-08-16016 August 1999 Forwards Proprietary TR WCAP-15128 & non-proprietary Rept WCAP-15129 for NRC Review.Repts Are Provided in Advance of TS Change That Is Being Prepared to Support Cycle 10 Rfo. Proprietary TR Withheld,Per 10CFR2.790 ML20210V1471999-08-13013 August 1999 Forwards Insp Repts 50-327/99-04 & 50-328/99-04 on 990601- 0717.One Potentially Safety Significant Issue Identified.On 990630,inadequate Performance of Storm Drain Sys Caused Water from Heavy Rainfall to Backup & Flood Turbine Bldg ML20211A1921999-08-12012 August 1999 Requests Proprietary TR WCAP-15128, Depth-Based SG Tube Repair Criteria for Axial PWSCC at Dented TSP Intersections, Be Withheld from Public Disclosure Per 10CFR2.790 ML20210Q5011999-08-0505 August 1999 Informs That NRC Plans to Administer Gfes of Written Operator Licensing Exam on 991006 at Sequoyah Nuclear Plant. Sample Registration Ltr Encl ML20210L4291999-08-0202 August 1999 Forwards Sequoyah Nuclear Plant Unit 2 Cycle 9 12-Month SG Insp Rept & SG-99-07-009, Sequoyah Unit-2 Cycle 10 Voltage-Based Repair Criteria 90-Day Rept. Repts Submitted IAW TS 4.4.5.5.b & TS 4.4.5.5.c ML20210L1611999-07-30030 July 1999 Forwards Request for Relief RV-4 Re ASME Class 1,2 & 3 Prvs, Per First ten-year Inservice Test Time Interval.Review & Approval of RV-4 Is Requested to Support Unit 1 Cycle 10 Refueling Outage,Scheduled to Start 000213 ML20210G5301999-07-28028 July 1999 Forwards Sequoyah Nuclear Plant Unit 2 ISI Summary Rept That Contains Historical Record of Repairs,Replacement & ISI & Augmented Examinations That Were Performed on ASME Code Class 1 & 2 Components from 971104-990511 ML20211B9661999-07-26026 July 1999 Informs That Sequoyah Nuclear Plant Sewage Treatment Plant, NPDES 0026450 Outfall 112,is in Standby Status.Flow Has Been Diverted from Sys Since Jan 1998 ML20210B2521999-07-14014 July 1999 Confirms 990712 Telcon Between J Smith of Licensee Staff & M Shannon of NRC Re semi-annual Mgt Meeting Schedule for 990820 in Atlanta,Ga to Discuss Recent Sequoyah Nuclear Plant Performance ML20210J1091999-07-10010 July 1999 Submits Suggestions & Concerns Re Y2K & Nuclear Power Plants ML20196K0381999-06-30030 June 1999 Provides Written Confirmation of Completed Commitment for Final Implementation of Thermo-Lag 330-1 Fire Barrier Corrective Actions at Snp,Per GL 92-08 ML20209E4071999-06-30030 June 1999 Forwards Insp Repts 50-327/99-03 & 50-328/99-03 on 990328- 0531.Violations Being Treated as Noncited Violations ML20196J8261999-06-28028 June 1999 Forwards Safety Evaluation Authorizing Request for Relief from ASME Boiler & Pressure Vessel Code,Section XI Requirements for Certain Inservice Inspections at Sequoyah Nuclear Plant,Units 1 & 2 ML20196G7881999-06-22022 June 1999 Informs NRC of Changes That Util Incorporated Into TS Bases Sections & Trm.Encl Provides Revised TS Bases Pages & TRM Affected by Listed Revs ML20196G1801999-06-21021 June 1999 Requests Termination of SRO License SOP-20751-1,for Lf Hardin,Effective 990611.Subject Individual Resigned from Position at TVA ML20195G1821999-06-0808 June 1999 Requests NRC Review & Approval of ASME Code Relief for ISI Program.Encl 1 Provides Relief Request 1-ISI-14 That Includes Two Attachments.Encl 2 Provides Copy of Related ASME Code Page ML20195E9521999-06-0707 June 1999 Requests Relief from Specific Requirements of ASME Section Xi,Subsection IWE of 1992 Edition,1992 Addenda.Util Has Determined That Proposed Alternatives Would Provide Acceptable Level of Quality & Safety ML20195E9311999-05-28028 May 1999 Informs of Planned Insp Activities for Licensee to Have Opportunity to Prepare for Insps & Provide NRC with Feedback on Any Planned Insps Which May Conflict with Plant Activities ML20195B3631999-05-21021 May 1999 Requests Termination of SRO License for Tj Van Huis,Per 10CFR50.74(a).TJ Van Huis Retired from Util,Effective 990514 ML20207A5721999-05-20020 May 1999 Forwards Correction to Previously Issued Amend 163 to License DPR-79 Re SR 4.1.1.1.1.d Inadvertently Omitted from Pp 3/4 1-1 of Unit 2 TS ML20206Q8791999-05-13013 May 1999 Forwards L36 9990415 802, COLR for Sequoyah Nuclear Plant Unit 2,Cycle 10, IAW Plant TS 6.9.1.14.c 05000327/LER-1999-001, Forwards LER 99-001-00 Re Condition That Resulted in Granting of Enforcement Discretion,Per Failure of Centrifugal Charging Pump.Condition Being Reported IAW 10CFR50.73(a)(2)(i)(B) & (a)(2)(iv)1999-05-11011 May 1999 Forwards LER 99-001-00 Re Condition That Resulted in Granting of Enforcement Discretion,Per Failure of Centrifugal Charging Pump.Condition Being Reported IAW 10CFR50.73(a)(2)(i)(B) & (a)(2)(iv) ML20206M9341999-05-10010 May 1999 Forwards Rept of SG Tube Plugging During Unit 2 Cycle 9 Refueling Outage,As Required by TS 4.4.5.5.a.ISI of Unit 2 SG Tubes Was Completed on 990503 ML20206K6271999-05-0606 May 1999 Requests Termination of SRO License for MR Taggart,License SOP-21336 Due to Resignation on 990430 ML20206J2061999-05-0404 May 1999 Requests Relief from Specified ISI Requirements in Section XI of ASME B&PV Code.Tva Requests Approval to Use Wire Type Penetrameters in Lieu of Plaque Type Penetrameters for Performing Radiographic Insps.Specific Relief Request,Encl ML20209J0391999-04-27027 April 1999 Forwards Annual Radioactive Effluent Release Rept, Radiological Impact Assessment Rept & Rev 41 to ODCM, for Period of Jan-Dec 1998 ML20206C6541999-04-23023 April 1999 Forwards Response to NRC 990127 RAI Re GL 96-05 for Sequoyah Nuclear Plant,Units 1 & 2 ML20206C0841999-04-23023 April 1999 Forwards Insp Repts 50-327/99-02 & 50-328/99-02 on 990214-0327.No Violations Noted ML20206B9591999-04-20020 April 1999 Responds to 990417 Request That NRC Exercise Discretion Not to Enforce Compliance with Actions Required in Unit 1 TS 3.1.2.2,3.1.2.4 & 3.5.2 & Documents 990417 Telephone Conversation When NRC Orally Issued NOED ML20205S5891999-04-17017 April 1999 Documents Request for Discretionary Enforcement for Unit 1 TS LCOs 3.1.2.2,3.1.2.4 & 3.5.2 to Support Completion of Repairs & Testing for 1B-B Centrifugal Charging Pump (CCP) 1999-09-07
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217M4461999-10-20020 October 1999 Forwards Rev 8 to Sequoyah Nuclear Plant Physical Security/ Contingency Plan, IAW 10CFR50.54(p).Encl Withheld,Per 10CFR73.21 05000327/LER-1999-002, Forwards LER 99-002-00 Re Start of Units 1 & 2 EDGs as Result of Cable Being Damaged During Installation of Thermo- Lag for Kaowool Upgrade Project1999-10-15015 October 1999 Forwards LER 99-002-00 Re Start of Units 1 & 2 EDGs as Result of Cable Being Damaged During Installation of Thermo- Lag for Kaowool Upgrade Project ML20217B8431999-10-0505 October 1999 Requests NRC Review & Approval of ASME Code Relief Requests That Were Identified in Plant Second 10-yr ISI Interval for Both Units.Encl 3 Provides Util Procedure for Calculation of ASME Code Coverage for Section XI Nondestructive Exams ML20217C7101999-10-0101 October 1999 Forwards Response to NRC 990910 RAI Re Sequoyah Nuclear Plant,Units 1 & 2 URI 50-327/98-04-02 & 50-328/98-04-02 Re Ice Weight Representative Sample ML20216J9351999-09-27027 September 1999 Responds to NRC Re Violations Noted in Insp Repts 50-327/99-04 & 50-328/99-04.Corrective Actions:Risk Determination Evaluation Was Performed & Licensee Concluded That Event Is in Green Regulatory Response Band ML20211N5681999-09-0101 September 1999 Submits Clarification of Two Issues Raised in Insp Repts 50-327/99-04 & 50-328/99-04,dtd 990813,which Was First Insp Rept Issued for Plant Under NRC Power Reactor Oversight Process Pilot Plant Study ML20211F8891999-08-25025 August 1999 Forwards Sequoyah Nuclear Plant Unit 1 Cycle 9 Refueling Outage, Re Completed SG Activities,Per TSs 4.4.5.5.b & 4.4.5.5.c ML20211A1851999-08-16016 August 1999 Forwards Proprietary TR WCAP-15128 & non-proprietary Rept WCAP-15129 for NRC Review.Repts Are Provided in Advance of TS Change That Is Being Prepared to Support Cycle 10 Rfo. Proprietary TR Withheld,Per 10CFR2.790 ML20211A1921999-08-12012 August 1999 Requests Proprietary TR WCAP-15128, Depth-Based SG Tube Repair Criteria for Axial PWSCC at Dented TSP Intersections, Be Withheld from Public Disclosure Per 10CFR2.790 ML20210L4291999-08-0202 August 1999 Forwards Sequoyah Nuclear Plant Unit 2 Cycle 9 12-Month SG Insp Rept & SG-99-07-009, Sequoyah Unit-2 Cycle 10 Voltage-Based Repair Criteria 90-Day Rept. Repts Submitted IAW TS 4.4.5.5.b & TS 4.4.5.5.c ML20210L1611999-07-30030 July 1999 Forwards Request for Relief RV-4 Re ASME Class 1,2 & 3 Prvs, Per First ten-year Inservice Test Time Interval.Review & Approval of RV-4 Is Requested to Support Unit 1 Cycle 10 Refueling Outage,Scheduled to Start 000213 ML20210G5301999-07-28028 July 1999 Forwards Sequoyah Nuclear Plant Unit 2 ISI Summary Rept That Contains Historical Record of Repairs,Replacement & ISI & Augmented Examinations That Were Performed on ASME Code Class 1 & 2 Components from 971104-990511 ML20210J1091999-07-10010 July 1999 Submits Suggestions & Concerns Re Y2K & Nuclear Power Plants ML20196K0381999-06-30030 June 1999 Provides Written Confirmation of Completed Commitment for Final Implementation of Thermo-Lag 330-1 Fire Barrier Corrective Actions at Snp,Per GL 92-08 ML20196G7881999-06-22022 June 1999 Informs NRC of Changes That Util Incorporated Into TS Bases Sections & Trm.Encl Provides Revised TS Bases Pages & TRM Affected by Listed Revs ML20196G1801999-06-21021 June 1999 Requests Termination of SRO License SOP-20751-1,for Lf Hardin,Effective 990611.Subject Individual Resigned from Position at TVA ML20195G1821999-06-0808 June 1999 Requests NRC Review & Approval of ASME Code Relief for ISI Program.Encl 1 Provides Relief Request 1-ISI-14 That Includes Two Attachments.Encl 2 Provides Copy of Related ASME Code Page ML20195E9521999-06-0707 June 1999 Requests Relief from Specific Requirements of ASME Section Xi,Subsection IWE of 1992 Edition,1992 Addenda.Util Has Determined That Proposed Alternatives Would Provide Acceptable Level of Quality & Safety ML20195B3631999-05-21021 May 1999 Requests Termination of SRO License for Tj Van Huis,Per 10CFR50.74(a).TJ Van Huis Retired from Util,Effective 990514 ML20206Q8791999-05-13013 May 1999 Forwards L36 9990415 802, COLR for Sequoyah Nuclear Plant Unit 2,Cycle 10, IAW Plant TS 6.9.1.14.c 05000327/LER-1999-001, Forwards LER 99-001-00 Re Condition That Resulted in Granting of Enforcement Discretion,Per Failure of Centrifugal Charging Pump.Condition Being Reported IAW 10CFR50.73(a)(2)(i)(B) & (a)(2)(iv)1999-05-11011 May 1999 Forwards LER 99-001-00 Re Condition That Resulted in Granting of Enforcement Discretion,Per Failure of Centrifugal Charging Pump.Condition Being Reported IAW 10CFR50.73(a)(2)(i)(B) & (a)(2)(iv) ML20206M9341999-05-10010 May 1999 Forwards Rept of SG Tube Plugging During Unit 2 Cycle 9 Refueling Outage,As Required by TS 4.4.5.5.a.ISI of Unit 2 SG Tubes Was Completed on 990503 ML20206K6271999-05-0606 May 1999 Requests Termination of SRO License for MR Taggart,License SOP-21336 Due to Resignation on 990430 ML20206J2061999-05-0404 May 1999 Requests Relief from Specified ISI Requirements in Section XI of ASME B&PV Code.Tva Requests Approval to Use Wire Type Penetrameters in Lieu of Plaque Type Penetrameters for Performing Radiographic Insps.Specific Relief Request,Encl ML20209J0391999-04-27027 April 1999 Forwards Annual Radioactive Effluent Release Rept, Radiological Impact Assessment Rept & Rev 41 to ODCM, for Period of Jan-Dec 1998 ML20206C6541999-04-23023 April 1999 Forwards Response to NRC 990127 RAI Re GL 96-05 for Sequoyah Nuclear Plant,Units 1 & 2 ML20205S5891999-04-17017 April 1999 Documents Request for Discretionary Enforcement for Unit 1 TS LCOs 3.1.2.2,3.1.2.4 & 3.5.2 to Support Completion of Repairs & Testing for 1B-B Centrifugal Charging Pump (CCP) ML20205B1091999-03-19019 March 1999 Submits Response to NRC Questions Concerning Lead Test Assembly Matl History,Per Request ML20204H0161999-03-19019 March 1999 Resubmits Util 990302 Response to Violations Noted in Insp Repts 50-327/98-11 & 50-328/98-11.Corrective Actions:Lessons Learned from Event Have Been Provided to Operating Crews ML20204E8251999-03-0505 March 1999 Forwards Sequoyah Nuclear Plant,Four Yr Simulator Test Rept for Period Ending 990321, in Accordance with Requirements of 10CFR55.45 ML20207E6851999-03-0202 March 1999 Responds to NRC Re Violations Noted in Insp Repts 50-327/98-11 & 50-328/98-11.Corrective Actions:Lessons Learned from Event Have Been Provided to Operating Crews ML20207J1171999-01-29029 January 1999 Forwards Copy of Final Exercise Rept for Full Participation Ingestion Pathway Exercise of Offsite Radiological Emergency Response Plans site-specific to Sequoyah NPP ML20202A7141999-01-20020 January 1999 Provides Request for Relief for Delaying Repair on Section of ASME Code Class 3 Piping within Essential Raw Cooling Water Sys ML20198S7141998-12-29029 December 1998 Forwards Cycle 10 Voltage-Based Repair Criteria 90-Day Rept, Per GL 95-05.Rept Is Submitted IAW License Condition 2.C.(9)(d) 05000327/LER-1998-004, Forwards LER 98-004-00,providing Details Concerning Inability to Complete Surveillance within Required Time Interval1998-12-21021 December 1998 Forwards LER 98-004-00,providing Details Concerning Inability to Complete Surveillance within Required Time Interval ML20198D5471998-12-14014 December 1998 Requests That License OP-20313-2 for Je Wright,Be Terminated IAW 10CFR50.74(a).Individual Retiring ML20197J5541998-12-10010 December 1998 Forwards Unit 1 Cycle 9 90-Day ISI Summary Rept IAW IWA-6220 & IWA-6230 of ASME Code,Section Xi.Request for Relief Will Be Submitted to NRC Timeframe to Support Second 10-year Insp Interval,Per 10CFR50.55a 05000327/LER-1998-003, Forwards LER 98-003-00 Re Automatic Reactor Trip with FW Isolation & Auxiliary FW Start as Result of Failure of Vital Inverter & Second Inverter Failure.Event Is Being Reported IAW 10CFR50.73(a)(2)(iv)1998-12-0909 December 1998 Forwards LER 98-003-00 Re Automatic Reactor Trip with FW Isolation & Auxiliary FW Start as Result of Failure of Vital Inverter & Second Inverter Failure.Event Is Being Reported IAW 10CFR50.73(a)(2)(iv) ML20196F9841998-11-25025 November 1998 Provides Changes to Calculated Peak Fuel Cladding Temp, Resulting from Recent Changes to Plant ECCS Evaluation Model ML20195H7891998-11-17017 November 1998 Requests NRC Review & Approval of Five ASME Code Relief Requests Identified in Snp Second ten-year ISI Interval for Units 1 & 2 ML20195E4991998-11-12012 November 1998 Forwards Rev 7 to Physical Security/Contingency Plan.Rev Adds Requirement That Security Personnel Will Assess Search Equipment Alarms & Add Definition of Major Maint.Rev Withheld (Ref 10CFR2.790(d)(1)) 05000328/LER-1998-002, Forwards LER 98-002-00 Re Automatic Turbine & Reactor Trip, Resulting from Failure of Sudden Pressure Relay on 'B' Phase Main Transformer1998-11-10010 November 1998 Forwards LER 98-002-00 Re Automatic Turbine & Reactor Trip, Resulting from Failure of Sudden Pressure Relay on 'B' Phase Main Transformer ML20195G5701998-11-10010 November 1998 Documents Util Basis for 981110 Telcon Request for Discretionary Enforcement for Plant TS 3.8.2.1,Action B,For 120-VAC Vital Instrument Power Board 1-IV.Licensee Determined That Inverter Failed Due to Component Failure ML20155J4031998-11-0505 November 1998 Provides Clarification of Topical Rept Associated with Insertion of Limited Number of Lead Test Assemblies Beginning with Unit 2 Operating Cycle 10 Core ML20154R9581998-10-21021 October 1998 Requests Approval of Encl Request for Relief ISI-3 from ASME Code Requirements Re Integrally Welded Attachments of Supports & Restraints for AFW Piping ML20155B1481998-10-21021 October 1998 Informs That as Result of Discussion of Issues Re Recent Events in Ice Condenser Industry,Ice Condenser Mini-Group (Icmg),Decided to Focus Efforts on Review & Potential Rev of Ice condenser-related TS in Order to Clarify Issues ML20154K1581998-10-13013 October 1998 Forwards Rept Re SG Tube Plugging Which Occurred During Unit 1 Cycle 9 Refueling Outage,Per TS 4.4.5.5.a.ISI of Unit 1 SG Was Completed on 980930 ML20154H6191998-10-0808 October 1998 Forwards Rev 0 to Sequoyah Nuclear Plant Unit 1 Cycle 10 COLR, IAW TS 6.9.1.14.c 05000328/LER-1998-001, Forwards LER 98-001-00 Providing Details Re Automatic Turbine & Reactor Trip Due to Failure of Sudden Pressure Relay on 'B' Phase Main Transformer1998-09-28028 September 1998 Forwards LER 98-001-00 Providing Details Re Automatic Turbine & Reactor Trip Due to Failure of Sudden Pressure Relay on 'B' Phase Main Transformer ML20151W4901998-09-0303 September 1998 Responds to NRC Re Violations Noted in Insp Repts 50-327/98-07 & 50-328/98-07.Corrective Actions:Revised Per SQ971279PER to Address Hardware Issues of Hysteresis, Pressure Shift & Abnormal Popping Noise 1999-09-27
[Table view] Category:UTILITY TO NRC
MONTHYEARML20059K6661990-09-17017 September 1990 Forwards Evaluation That Provides Details of Plug Cracks & Justification for Continued Operation Until 1993 ML20059H4031990-09-10010 September 1990 Discusses Plant Design Baseline & Verification Program Deficiency D.4.3-3 Noted in Insp Repts 50-327/86-27 & 50-328/86-27.Evaluation Concluded That pre-restart Walkdown Data,Loops 1 & 2 Yielded Adequate Design Input ML20059E1851990-08-31031 August 1990 Responds to NRC Re Violations Noted in Insp Repts 50-327/90-22 & 50-328/90-22.Corrective Actions:Extensive Mgt Focus Being Applied to Improve Overtime Use Controls ML20059E2881990-08-31031 August 1990 Forwards Addl Info Re Alternate Testing of Reactor Vessel Head & Internals Lifting Rigs,Per NUREG-0612.Based on Listed Hardships,Util Did Not Choose 150% Load Test Option ML20059H1831990-08-31031 August 1990 Forwards Nonproprietary PFE-F26NP & Proprietary PFE-F26, Sequoyah Nuclear Plan Unit 1,Cycle 5 Restart Physics Test Summary, Re Testing Following Vantage 5H Fuel Assembly installation.PFE-F26 Withheld (Ref 10CFR2.790(b)(4)) ML18033B5031990-08-31031 August 1990 Forwards Financial Info Required to Assure Retrospective Premiums,Per 10CFR140 & 771209 Ltr ML20028G8341990-08-28028 August 1990 Forwards Calculation SCG1S361, Foundation Investigation of ERCW Pumping Station Foundation Cells. ML20063Q2471990-08-20020 August 1990 Submits Implementation Schedule for Cable Tray Support Program.Util Proposes Deferral of Portion of Remaining Activities Until After Current Unit 2 Cycle 4 Refueling Outage,Per 900817 Meeting.Tva Presentation Matl Encl ML20056B5181990-08-20020 August 1990 Responds to NRC Re Order Imposing Civil Monetary Penalty & Violations Noted in Insp Repts 50-327/90-01 & 50-328/90-01.Corrective Actions:Organizational Capabilities Reviewed.Payment of Civil Penalty Wired to NRC ML20063Q2461990-08-17017 August 1990 Forwards Cable Test Program Resolution Plan to Resolve Issues Re Pullbys,Jamming & Vertical Supported Cable & TVA- Identified Cable Damage.Tva Commits to Take Actions Prior to Startup to Verify Integrity of safety-related Cables ML20059A5121990-08-15015 August 1990 Provides Clarification of Implementation of Replacement Items Project at Plant for Previously Procured Warehouse Inventory.Util Committed to 100% Dedication of Commercial Grade,Qa,Level Ii,Previous Procurement Warehouse Spare ML20058M2321990-08-0707 August 1990 Forwards Rept of 900709 Fishkill,Per Requirements in App B, Environ Tech Spec,Subsections 4.1.1 & 5.4.2.Sudden Water Temp Increase Killed Approximately 150 Fish in Plant Diffuser Pond ML20058N2361990-08-0707 August 1990 Confirms That Requalification Program Evaluation Ref Matl Delivered to Rd Mcwhorter on 900801.Ref Matl Needed to Support NRC Preparation for Administering Licensed Operator Requalification Exams in Sept 1990 ML20058M4471990-07-27027 July 1990 Responds to Unresolved Items Which Remain Open from Insp Repts 50-327/90-18 & 50-328/90-18.TVA in Agreement W/Nrc on Scope of Work Required to Address Concerns W/Exception of Design Basis Accident & Zero Period Accelaration Effects ML20058M0111990-07-27027 July 1990 Forwards Addl Info Re Plant Condition Adverse to Quality Rept Concerning Operability Determination.Probability of Cable Damage During Installation Low.No Programmatic Cable Installation Problems Exist ML20055J3531990-07-27027 July 1990 Forwards Revised Commitment to Resolve EOP Step Deviation Document Review Comments ML20055J0771990-07-26026 July 1990 Requests Termination of Senior Reactor Operator License SOP-20830 for Jh Sullivan Due to Resignation from Util ML20055G6611990-07-17017 July 1990 Forwards Justification for Continued Operation for safety- Related Cables Installed at Plant,Per 900717 Telcon.No Operability Concern Exists at Plant & No Programmatic Problems Have Been Identified.Summary of Commitments Encl ML20058L7001990-07-16016 July 1990 Forwards Response to SALP Repts 50-327/90-09 & 50-328/90-09 for 890204 - 900305,including Corrective Actions & Improvements Being Implemented ML20055F6151990-07-13013 July 1990 Provides Addl Bases for Util 900320 Proposal to Discontinue Review to Identify Maint Direct Charge molded-case Circuit Breakers Procured Between Aug 1983 & Dec 1984,per NRC Bulletin 88-010.No Significant Assurance Would Be Expected ML20044B2211990-07-12012 July 1990 Forwards Addl Info Clarifying Certain Conclusions & Recommendation in SER Re First 10-yr Interval Inservice Insp Program ML20055D2531990-07-0202 July 1990 Provides Status of Q-list Development at Plant & Revises Completion Date for Effort.Implementation of Q-list Would Cause Unnecessary & Costly Delays in Replanning Maint,Mod, outage-related Activities & Associated Procedure Revs ML20043H9061990-06-21021 June 1990 Responds to Generic Ltr 90-04, Request for Info on Status of Licensee Implementaion of Generic Safety Issues Resolved W/Imposition or Requirements or Corrective Actions. No Commitments Contained in Submittal ML20043H2281990-06-18018 June 1990 Informs of Issue Recently Identified During Startup of Facility from Cycle 4 Refueling Outage & How Issue Addressed to Support Continued Escalation to 100% Power,Per 900613 & 14 Telcons ML20043G4901990-06-14014 June 1990 Forwards Tabs for Apps a & B to Be Inserted Into Util Consolidated Nuclear Power Radiological Emergency Plan ML20043F9261990-06-13013 June 1990 Responds to NRC Bulletin 89-002, Stress Corrosion Cracking of High-Hardness Type 410 Stainless Steel Internal Preloaded Bolting in Anchor/Darling Model S3502 Swing Check Valves or Valves of Similar Design. ML20043F9301990-06-13013 June 1990 Responds to NRC 900516 Ltr Re Violations Noted in Insp Repts 50-327/90-17 & 50-328/90-17.Corrective Action:Test Director & Supervisor Involved Given Appropriate Level of Disciplinary Action ML20043H0361990-06-11011 June 1990 Forwards Supplemental Info Re Unresolved Item 88-12-04 Addressing Concern W/Double Differentiation Technique Used to Generate Containment Design Basis Accident Spectra,Per 900412 Request ML20043D9921990-06-0505 June 1990 Responds to NRC 900507 Ltr Re Violations Noted in Insp Repts 50-327/90-14 & 50-328/90-14.Corrective Actions:Util Reviewed Issue & Determined That Trains a & B Demonstrated Operable in Jan & Apr,Respectively of 1989 ML20043C2821990-05-29029 May 1990 Requests Relief from ASME Section XI Re Hydrostatic Pressure Test Requirements Involving RCS & Small Section of Connected ECCS Piping for Plant.Replacement & Testing of Check Valve 1-VLV-63-551 Presently Scheduled for Completion on 900530 ML20043C0581990-05-29029 May 1990 Forwards Response to NRC 900426 Ltr Re Violations Noted in Insp Repts 50-327/90-15 & 50-328/90-15.Response Withheld (Ref 10CFR73.21) ML20043B3051990-05-22022 May 1990 Forwards Detailed Scenario for 900711 Radiological Emergency Plan Exercise.W/O Encl ML20043B1201990-05-18018 May 1990 Forwards, Diesel Generator Voltage Response Improvement Rept. Combined Effect of Resetting Exciter Current Transformers to Achieve flat-compounding & Installing Electronic Load Sequence Timers Produced Acceptable Voltage ML20043A6101990-05-15015 May 1990 Forwards Rev 16 to Security Personnel Training & Qualification Plan.Rev Withheld (Ref 10CFR2.790) ML20043A2391990-05-15015 May 1990 Forwards Revised Tech Spec Pages to Support Tech Spec Change 89-27 Re Steam Generator Water Level Adverse Trip Setpoints for Reactor Trip Sys Instrumentation & Esfas. Encl Reflects Ref Leg Heatup Environ Allowance ML20043A0581990-05-11011 May 1990 Forwards Cycle 5 Redesign Peaking Factor Limit Rept for Facility.Unit Redesigned During Refueling Outage Due to Removal & Replacement of Several Fuel Assemblies Found to Contain Leaking Fuel Rods ML20043A0571990-05-10010 May 1990 Forwards List of Commitments to Support NRC Review of Eagle 21 Reactor Protection Sys Function Upgrade,Per 900510 Telcon ML20042G9771990-05-0909 May 1990 Responds to NRC 900412 Ltr Re Violations Noted in Insp Repts 50-327/90-01 & 50-328/90-01 & Proposed Imposition of Civil Penalty.Corrective Actions:Rhr Pump 1B-B Handswitch in pull- to-lock Position to Ensure One Train of ECCS Operable ML20042G4651990-05-0909 May 1990 Provides Addl Info Re Plant Steam Generator Low Water Level Trip Time Delay & Function of P-8 Reactor Trip Interlock,Per 900430 Telcon.Trip Time Delay Does Not Utilize P-8 Interlock in Any Manner ML20042G4541990-05-0909 May 1990 Provides Notification of Steam Generator Tube Plugging During Unit 1 Cycle 4 Refueling Outage,Per Tech Specs 4.4.5.5.a.Rept of Results of Inservice Insp to Be Submitted by 910427.Summary of Tubes Plugged in Unit 1 Encl ML20042G0441990-05-0808 May 1990 Forwards Nonproprietary WCAP-11896 & WCAP-8587,Suppl 1 & Proprietary WCAP-8687,Suppls 2-E69A & 2-E69B & WCAP-11733 Re Westinghouse Eagle 21 Process Protection Sys Components Equipment Qualification Test Rept.Proprietary Rept Withheld ML20042G1431990-05-0808 May 1990 Forwards WCAP-12588, Sequoyah Eagle 21 Process Protection Sys Replacement Hardware Verification & Validation Final Rept. Info Submitted in Support of Tech Spec Change 89-27 Dtd 900124 ML20042G1001990-05-0808 May 1990 Forwards Proprietary WCAP 12504 & Nonproprietary WCAP 12548, Summary Rept Process Protection Sys Eagle 21 Upgrade,Rtd Bypass Elimination,New Steam Line Break Sys,Medical Signal Selector .... Proprietary Rept Withheld (Ref 10CFR2.790) ML20042G1701990-05-0808 May 1990 Provides Addl Info Re Eagle 21 Upgrade to Plant Reactor Protection Sys,Per 900418-20 Audit Meeting.Partial Trip Output Board Design & Operation Proven by Noise,Fault,Surge & Radio Frequency Interference Testing Noted in WCAP-11733 ML20042G1231990-05-0707 May 1990 Forwards Detailed Discussion of Util Program & Methodology Used at Plant to Satisfy Intent of Reg Guide 1.97,Rev 2 Re Licensing Position on post-accident Monitoring ML20042F7741990-05-0404 May 1990 Informs of Completion of Eagle 21 Verification & Validation Activities Re Plant Process Protection Sys Upgrade.No Significant Disturbances Noted from NRC Completion Date of 900420 ML20042F1691990-05-0303 May 1990 Responds to NRC Bulletin 88-009, Thimble Tube Thinning in Westinghouse Electric Corporation Reactors. Wear Acceptance Criteria Established & Appropriate Corrective Actions Noted. Criteria & Corresponding Disposition Listed ML20042G1381990-04-26026 April 1990 Forwards Westinghouse 900426 Ltr to Util Providing Supplemental Info to Address Questions Raised by NRC Re Eagle-21 Process Protection Channels Required for Mode 5 Operation at Facilities ML20042E9641990-04-26026 April 1990 Forwards Rev 24 to Physical Security/Contingency Plan.Rev Withheld (Ref 10CFR73.21) ML20012E6181990-03-28028 March 1990 Discusses Reevaluation of Cable Pullby Issue at Plant in Light of Damage Discovered at Watts Bar Nuclear Plant. Previous Conclusions Drawn Re Integrity of Class 1E Cable Sys Continue to Be Valid.Details of Reevaluation Encl 1990-09-17
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TENNESSEE VALLEY ' AUTHORITY CH ATTANOOGA. T ENNESSFE 37401 SN 1578 Lookout Place JUL 051988 Olrector, Office of Enforcement U.S. Nuclear Regulatory Commission ATIN: . Document Control Desk Washington, D.C. 20555 Gentlemen:
In the Matter of ) Docket No. 50-328 Tennessee Valley Authority )
SEQUOYAH NUCLEAR PLANT (SQN) UNIT 2 - NOTICE OF VIOLATION AND PROPOSED IMPOSITION OF CIVIL PENALTY (NRC INSPECTION REPORT NO. 50-328/88-20) -
RESPONSE TO NOTICE OF VIOLATION Enclosed is TVA's response to S. D. Ebneter's letter to S. A. White dated June 3 1988, that transmitted two notices of violation and proposed imposition of civil penalty and two violations not assessed a civil penalty (NRC Inspection Report No. 50-328/88-20).
Enclosure 1 provides TVA's response to the notices of violation assessed a "
civil penalty. Enclosure 2 provides TVA's response to notices of violation not assessed a civil penalty. Sumnary statements of commitments contained in this submittal are provided in enclosure 3.
I Fees in response to the civil penalty of $50,000 are being wired to NRC, I attention Director, Office of Enforcement.
t i
.If you have any questions, please telephone me at (615) 751-2729.
Very truly yours, l TENNESSEE V LLEY AUTHORITY R. rid ey, O ector -
Nuclear Licensing and Regulatory Affairs Enclosures cc: See page 2 l
[
l l l -
8807080016 880705 PDR ADOCK 05000328 Q PDC m An Equal opportunity Employer
s .
i U.S. Nuclear Regulatory Commission JUL 051988 cc (Enclosures):
Mr. F. R. McCoy, Assistant Director for Inspection Programs TVA Projects Division U.S. Nuclear Regulatory Commission Region II 101 Harletta Street, NH, Suite 2900 Atlanta, Georgia 30323 Ms. S. C. Black, Assistant Director for Projects TVA Projects Division U.S. Nuclear Regulatory Commission One White Flint, North 11555 Rockville Pike Rockville, Maryland 20852 Sequoyah Resident Inspector Sequoyah Nuclear Plant 2600 Igou Ferry Road Soddy Daisy, Tennessee 37379
i
. ENCLOSURE 1 RESPCNSE TO NRC INSPECTION REPORT NUMBER 50-328/88-20 REPLY TO A NOTICE OF VIOLATJ0N
~
PROPOSE 0 CIVIL PENALTY S. D. EBNETER'S LETTER TO S. A. WHITE DATED JUNE 3, 1988 Violation 50-328/88-20.I.A "I. Violations Assessed a Civil Penalty A. Technical Specification 3.5.2 requires for MODES 1, 2, and 3, a minimum of two independent emergency core cooling system (ECCS) subsystems shall be operable with each subsystem comprised of, among otner equipmert, one operable centrifugal charging pump.
Technical Specification 3.0.3, which contains the ACTION requirements when two ECCS subsystems are inoperable, requires, in part, that within one hour, action shall be initiated to place the unit in a MODE in which the Specification does not apply.
Contrary to the above, on March 9, 1988, with the unit in MODE 3, two ECCS subsystems were inoperable for one hour and twenty-four minutes and action was not initiated to place the unit in a MODE in which the Specification does not apply. Both centrifugal charging pumps were in the pull-to-lock position and would not have operated automatically upon receipt of a safety injection signal."
Admission or Denial of the Alleged Violation TVA admits the violation subject to the following corrections and clarification. During the I hour 24 minutes in question, the handswitch (HS) for the 28-8 centrifugal :harging pump (CCP) was not in the pull-to-lock (PTL) position. Maintenance had previously been completed on the 28-8 pump, and the pump had been returned to service and was in service providing charging flow and RCP seal flow. However, the postmaintenance test (PMT) had rot yet been completed; and therefore the 28-B pump was not technically declared operable at that time. The 28-B CCP would have operated automatically upon receiving a safety injection signal. The 2A-A CCP HS was in the PTL position as discussed below.
Reason for the Violation The immediate causes of the violation were a result of the day-shif t reactor operator (RO) (operator A) not recognizing that placing the CCP HS in the PTL position would result in the CCP being considered inopeiabie. The 28.B CCP, for which maintenance had previously been completed, was placed in service to perform a PMT. The 2A-A CCP HS was placed in the PTL position. The PMT on 28-B was completed I hour and 24 minutes later, and the 2B-B CCP was lef t in service with the 2A-A CCP HS still in the PTL position. Because of the operator's (operator B) interpretation of the switch position and a high level of activity in the Main Control Room (MCR) during the turnover process, the subsequent shift turnover did not identify that the 2A-A pump was inoperable
.as a result of the HS being in the PTL position. Because the turnover process l
r
, did not identify the 2A-A CCP as being inoperable,.the HS position was incorrectly logged in the System Status Checklist (Appendix B1) of Administrative Instruction (AI) 5, "Shift Relief and Turnover."
During a nonscheduled shift turnover, a new system status checklist (Appendix B1 of AI-5) was not completed by operhtor C; and the incorrectly posttioned CCP HS was not identified at that time. The incorrectly positioned CCP HS was subsequently identified by an NRC inspector, and the HS was then returned to the A-Auto position. During the initial 1-hour-24-minute period, the 2A-A CCP HS was in the PTL position and the 28-B CCP was technically inoperable because of a PMT being performed. However, the 28-B pump was in service and operating during this period with the HS in the A-Auto position. Subsequent completion of the PMT indicated that, had an accident occurred, the 2B-8 pump would have operated automatically to provide required emergency core cooling.
The root causes of the violation resulted from management not adequately considering the potential effects of temporarily assigning operators to a cold shutdown unit and back to an operating unit (mode 3). Operator A had recently been transferred from unit I to unit 2 before this event. This contributed to the operator not fully refocusing to more restrictive technical specification (TS) requirements, to thinking operability requirements were being met with the CCP HS in the PTL position as previously permitted in cold shutdown for reactivity control considerations, and to automatically placing the nonrunning pump in PTL as required in modes 4 and 5 for cold overpressurization considerations. Also, management direction regarding detail of operator log entries and operator communication were less than fully adequate, thus allowing a misleading log entry on the status of CCP-2A-A that resulted in a failure to communicate abnormal status of safety-related equipment.
In addition to the above, procedural weaknesses contributed to failure to recognize the situation. Al-5 did not adequately address nonscheduled shift turnovers. This resulted in the evening shift relief (operator C) not performing a new, independent Appendix Bl to Al-5. An existing TS interpretation (TSI) concerning the operability of a CCP in the PTL position was not consistent with current plant management philosophy. A discrepancy existed between section B of General Operating Instruction (GOI) 3, "Plant Shutdown from Minimum Load to Cold Shutdown," (precaution for solid water operation) and TS 3.1.2.4 (CCPs needed for reactivity control). G01-3 requires one CCP to be locked out when reactor coolant system (RCS) temperature is less than 350 degrees Fahrenheit, node 4, while TS 3.1.2.4 requires both CCPs to be operable in nodes 1 through 4. These procedural weaknesses partly contributed to operator perception that the 2A-A pump was operable with the HS in PTL and failure to identify and question the abnormal HS position.
L Corrective Steps That Have 8een Taken and Results Achieved i The 28-8 CCP was declared operable following PMT, and limiting condition for operation (LCO) 3.0.3 was exited. The 2A-A CCP HS was placed in the A-Auto position upon identification, therefore exiting LCO 3.5.2.
s TVA has instituted extensive corrective actions to prevent recurrence of this event. These actions include changes to plant procedures, additional administrative controls, increased operator training, and a formal review of TSIs currently in use. The following lists the specific actions completed by TVA to date.
- 1. Controls have been established to limit interchanging operators from a cold shutdown unit to an operating unit. Approval to interchange must come from the plant manager.
- 2. AI-6, "Log Entries and Review," (for operator log entries) has been revised to delineate the level of detail for log entries such as specifying switch positions.
- 3. AI-30, "Nuclear Plant Conduct of Operation," (for operator communication) has been revised to increase the level of communication among operators by specifying interface requirements that must be satisfied during control board manipulations that relate to changing switch positions or taking major equipment out of service.
- 4. AI-5 has been revised to require the completion of an Appendix B1 l checklist for nonscheduled shift relief.
- 5. A review of for.nal SQN TSIs has been performed for techni:a1 adequacy and clarity. TSIs needing changes have been corrected.
- 6. AI-5 has been revised to require the unit supervisor senior reactor operator (SRO) to observe the main control board status for abnormal conditions before assuming shift. A checklist-type guidance is provided, and the review is documented in the unit supervisor log.
- 7. Senior Office of Nuclear Power tranagement has addressed Operations personnel on the causes, conclusions, and corrective actions for this event.
- 8. Signs to emphasize plant operating mode have been placed in the MCR and auxiliary instrument room.
- 9. Training has been completed on procedure changes and TSI changes for unit 2 operators.
- 10. Scenarios emphasizing the use of TSs have been incorporated into the operator simulator training program. Training sessions with unit 2 licensed operators have been conducted.
- 11. The requirement in G01-3, to place one CCP HS-in the PTL position below 350 degrees Fahrenhelt, has been revised to pefform the action of PTL upon entry into mode 5. Revision 37 was approved May 13, 1988. .
- 12. TS 3.5.3, mode 4, and 3.1.2.4, modes 1-4, have been evaluated and determined to be consistent.
Corrective Steps That Will Be Taken to Avoid Further Violations
- 1. Training for unit 1 operators will be given on procedure changes and TSI changes before unit 1 enters mode 2 as committed to in Licensee Event Report (LER) SQRO-50-328/88010.
- 2. Scenarios emphasizing the use of TSs have been incorporated into operator simulator training. Training for unit 1 operators will be completed before unit i enters mode 2 as committed to in LER SQRO-50-328/88010.
- 3. Corresponding changes to the Final Safety Analysis Report, section 5.2.2.4.4, regarding administrative procedures for RCS pressure control during low-temperature operation will be submitted in the next annual update.
Date When Full Compilance Will Be Achieved TVA is in full compliance.
Violation 50-328/88-20.I.8
, "B. 10 CFR 50.72.b.2.111 requires the reporting to the NRC Operations Center via the Emergency Notification System (Red Phone) within four hours of eccurrence, any event or condition that alon! could have prevented the fulfillment of the safety functiu of structures or systems that are needed to shut down the reactor and maintain it in a j safe shutdown condition, remove residual heat, control the release of l
radioactive material, or mitigate the consequences of an accident.
) Contrary to the above, on March 9, 1988, the inoperability of the centrifugal charging pumps was not re,.orted to the NRC Operations Center within the required four hours after it was identified.
! Collectively, those violations have been categorized in the aggregate as a Severt ty Level III problem (Supplement I).
Cumulative Civil Penalty - $50,000 (assessed equally between the violations),"
l Admission or Denial of the /.lleged Violation TVA admits the violation.
Reason for the Violation - ,
On March 9, 1988, at approximately 2000 eastern standard time, the shift operation supervisor (SOS) was made aware of the 2A-A CCP HS having been in the PTL position. The SOS assessed the event along with the shift technical advisor, and a potential reportable occurrence was written. At this time, the SOS did not have positive evidence that the 2A-A CCP was inoperable as a result of being in PTL coincident with the 2B-B CCP undergoing a PMT earlier that day. Following verification the following morning with the operators involved that the 2A-A CCP HS had been in the PTL position coincident with~the PMT on the 28-B CCP and.that this condition had lasted for 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> 24 minutes, it was concluded that TS LCO 3.0.3 had been inadvertently entered. Because this situation was not recognized at the time, a shutdown had not been initiated within one hour, resulting in an operation prohibited by TSs. This would be reportable to NRC in accordance with 10 CFR 50.73.a.2.1.8 (LER). In an effort to keep NRC apprised of activities at SQN, a conservative application of 10 CFR 50.72 was also applied; and the four hour notification was effected. ,
TVA does not wish to pursue this specific event further; however, in reviewing the overall issue with respect to NRC guidelincs for reporting, it is unclear that the event in itself meets any of the re'luirements of 10 CFR 50.72 rules.
It does, however, meet the requirements of 10 CFR 50.73 for a 30-day LER in accordance with 10 CFR 50.73.a.2.1 as an operation prohibited by the TSs. The event was conservatively reported as a four hour notification under the 10 CFR 50.72.b.2.111 rule. This rule addresses any event or condition that alone could have prevented the fulfillment of safety functions. This rule "
does not require that you assume a failure of the opposite train.
Specifically, NUREG-1022, Supplement 1, question 7.8, states that unrelated, independent failures that did not actually occur should not be included in the evaluation if an event or condition is reportable under this rule. During this event, the 28-B CCP was in operation, as was stated earlier, and was always capable of performing its intended safety function. Had an accident occurred during this time, the 28-B CCP would have continued to operate and ;
perform its emergency core cooling function. ;.
l' In conclusion, a notification was not made to NRC within four hours of the identification of the 2A-A CCP HS in the PTL position; but it is believed that a conservative interpretation of the reporting requirements was made upon confirmation that TS 3.0.3 had inadvertently been ent; red and confirmation i that the duration resulted in the action of TS 3.0.3 not being compiled with. '
Corrective Steps That Have B?en Taken Immediate corrective actions were effected by making the telephone l; notification. TVA senior management has directed the shift supervisors te i ensure control of shift activities and to become more involved with incidents -
of this nature. The 50Ss are aware of their responsibility to perform ll determinations and notifications in accordance with 10 CFR 50.72.
J
TVA management has additionally discussed with the.50Ss the importance of aggressively pursuing resolutions in a timely fashion of incidents involving TSs. TVA management has also directed the SOSs to be conservative during evaluations of events involving TSs and to initiate a notification when situations indicate this action could be required.
Corrective Steps That Will Be Taken to Avoid Further Violations No further action is required.
Date When Full Compliance Will Be Achieved TVA is in full compliance.
4
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/
ENCLOSURE 2 RESPONSE TO NRC INSPECTION REPORT NUMBER 50-328/88-20 REPLY TO A NOTICE OF VIOLATION NOT ASSESSED A CIVIL PENALTY S. D. EBNETER'S LETTER TO S. A. WHITE DATED JUNE 3, 1988 Violation 50-328/88-20.II.A "II. Violations Not Assessed a Civil Penalty A. Technical Specification 6.8.1 requires that written procedures be establishe'd, implemented, and maintainee' covering the applicable procedures recommended in Appendix A of Regulatory Guide 1.33, ,
Revision 2, February 1978. Appendix A o' Regulatory Guide 1.33 requires that procedures be established and implemented to control system operations and administrative acti"ities.
Contrary to the above, the licensee failed to adequately establish and implement procedures in the following instances:
- 1. On March 5, 1988, a Technical Specification Interpretation was established and used that conflicted with the plant Technical Specifications. Technical Specification Interpretation 8 allowed operation of the facility, with Technical Specification 3.0.5 invoked, with one alternate motor driven auxiliary feedwater train operable and the capability to supply at least three steam generators from the turbine driven 4
auxiliary feedwater pump. In some circumstances, this allowed 3 operation of the facility with flow paths to only three steam generators. However, Technical Specification 3.7.1.2 requires that flow paths to all four steam generators be operable.
- 2. On March 9, 1988, the improper implementation of the AI-5 Lead Operator Checklist resulted in the improper documentation of the 2A-A CCP control room handswitch position. The checklist Indicated that the handswitch was in the prcper position (i.e. A-Auto), whereas the actual position w. pull-to-lock 3 (PTL).
This is a Severity Level IV violation (supplement I)."
Admission or Denial of the Alleged Violation (example 1)
TVA admits the violation.
Reason for the Violation On March 5,1988, during the performance of Sur..'111ance :nstructior, (SI) 166.8, "Increased Frequency Testing of Category A and 8 Valves," valve 2-LCV-3-175 failed to stroke. 51 14' J reluir.;s that, if the valve exceeds the maximum allowable stroke time u've sh '
he declared inoperable and
! repaired. The valvt should have red insperable end LC0 3.7.1.2
- entered; but the operator usad
- the operation of unit 2 without entry into an LCO. Additional' .
~ the valve .o strcka was not ;
recorded in the 509, UO, or R0 '
gy .mw ,,..%.m,, , - -- --
The root cause of this violation was failure to properly implement SI-166.8 is written, failure to record the occurrence in operational logs at the time of the event, and use of an inadequate TSI resulting in failure to enter an LCO, Corrective Steps That Have Been Taken and Results Achieved
- 1. AI-6 has been revised to delineate the level of detail for log entries.
- 2. A rev u / of formal SQN TSIs has been performed for technical adequacy arf clarity. TSIs needing changes have been corrected.
- 3. Scenarios emphasizing the use of TSs have been incorporated into the operator simulator training program.
- 4. Late entries were written in 505/UO/R0 logs to reflect the findings of valve nonactuation by the previous shifts.
Corrective Action That Will Be Taken to Avoid Further Violations No further corrective action is required.
Date When Full Compliance Hill Be Achieved TVA is in full compliance.
Admission or Denial of the Alleged Violation (example 2)
TVA admits the violation.
Reason for the Violation The HS for 2A-A CCP was placed in the PTL position by the day-shift R0 (operator A) when the 28-B CCP was placed in service to perform a PMT.
Because of the operator's (operator B) interpretation of the switch position and a high level of activity occurring in the MCR during the turnover process, the subsequent shift turnover did not identify that the 2A-A pump was inoperable as a result of the HS being in the PTL position. Bec:Use the turnover process did not identify the 2A-A CCP as being inoperable, the HS position was incorrectly logged in the System Status Checklist (Appendix B1) of AI-S.
m - . i l
Corrective Steps That Have Been Taken and Results Achieved- >
- 1. AI-6 (for operator log entries) has been revised to delineate the level of I detall for log entries such as specifying switch positions. ;
- 2. . AI-30 (for operator communication) has been revised to increase the level of communication among operators by specifying interface requirements that must be satisfied during control board manipulations that relate to ,
changing switch positions or taking major equipment out of service. !
l
- 3. AI-5 has been revised to require the unit supervisor SR0 to observe the j main control board status for abnormal conditions before assuming shift.
A checklist-type guidance is providec, and the review is documented in the unit supervisor log.
. Corrective Steps That Will Be Taken to Avoid Further Violations, No #urther action is required.
- Date When Full Compliance Will Be Achieved TVA is in full compilance.
Violation S0-328/88-20.11.B "B. TS 4.5.1.1.1.6 requires that each cold leg accumulator be demonstrated l
operable by verifying the boron concentration within six_ hours after i each solution volume increase of greater than or equal to 1 percent of l
- the tank volume. '
Contrary to the above, on March 6, 1988, the number 3 cold leg accumulator boron concentration was not verified within six hours after a solution volume increase of greater that I percent of tank I volume due to inleakage.
l This is a Severity Level IV violation (Supplement I)."
! Admission or Dental of the Alleged Violation ,
i
! TVA admits the violation. ;
Reason for the Violation i I i l The root causes of this violation have been determin.J to be that the Operations shift crews did not consider that the RCS leakage into the i accumulator, after draining the accumulator, constituted a filling operation j and that applicable Operations procedures did not alert the op?rator to l
l request a boron concentration sample for such an event, i
l ,
I
I'
' Corrective Steps That Have Been Taken and Results Achieved Immediate corrective actions were to declare the accumulator inoperablo and to have the Radiochemistry Laboratory verify the boron concentration.
Radiochemistry Laboratory personnel sampled the accumulator; and the results of the sample yielded a boron concentration of 2,085 parts per million, which is within TS limits. The accumulator was then declared operable.
In order to preclude recurrence of the event, System Operating Instruction 63.1, "Emergency Core Cooling System," has been revised to require a boron concentration sample to be taken af ter both filling and draining occur. This will prevent refilling of the accumulator without obtaining the corresponding boron concentration as required by TSs. A training letter has been issued to Operations personnel detalling the subject matter of this incident. This will ensure that operators are aware that inleakage into a tank or accumulator constitutes a refilling operation and that appropriate action must be
. initiated. Additionally, SI-2, "Shif t Log," contains a note that will alert Operations personnel to notify the Radiochemistry Laboratory to perform a boron concentration analysis when cold-leg accumulator volume increases by 1 percent or greater, as recuired by TSs.
Corrective Steps That Hill Be Taken to Avoid Further Violations No further corrective action is required.
Date When Full Compliance Hill Be Achieved TVA-is in full compliance.
1 g
r "0SURE 3
,, Commitments
- 1. Training for ur. ,c.atorswillbegivenonhrocedurechangesandTSI changes before unit i enters mode 2 as committed to in LER SQRO-50-328/88010.
- 2. Scenarios emphasizing the use of TSs have been incorporated into operator simulator training. Training for Unit 1 operators will be completed before unit i enters mode 2 as committed to in LER SQR0-50-328/88010.
- 3. Corresponding changes to the Final Safety Analysis Report, section 5.2.2.4.4, will be submitted in the next. annual update.