ML20206M934

From kanterella
Jump to navigation Jump to search
Forwards Rept of SG Tube Plugging During Unit 2 Cycle 9 Refueling Outage,As Required by TS 4.4.5.5.a.ISI of Unit 2 SG Tubes Was Completed on 990503
ML20206M934
Person / Time
Site: Sequoyah 
Issue date: 05/10/1999
From: Salas P
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9905170084
Download: ML20206M934 (4)


Text

.

1 Iennessee variey Aumonty Post OHice Box 7 c ddy Daisy Tennessee 37379 May 10, 1999 U.S.

Nuclear Regulatory Commission ATTN:

Document Control Desk Washington, D.C.

20555 Gentlemen:

In the Matter

)

Docket No. 50-328 Tennessee Valley Authority

)

SEQUOYAH NUCIJZAR PLANT (SQN) - UNIT 2 STEAM GENERATOR (SG)

TUBE PLUGGING REPORT AND NOTIFICATION OF UNIT 2 SG TUBE INSPECTIONS - UNIT 2 CYCLE 9 REFUELING OUTAGE As required by SON Technical Specification (TS) 4.4.5.5.a, this submittal provides a report of SG tube plugging during l

the Unit 2 Cycle 9 refueling outage.

The report is included l

in the enclosure.

The in-service inspection (ISI) of the Unit 2 SG tubes was completed on May 3, 1999.

Pursuant to the reporting requirements of TS 4.4.5.5.c, NRC was notified of the SG tube inspections that fell into Category C-3.

Notification of these results was made during l

a telephone conference call on May 3, 1999.

In accordance l

with SON TS 3/4.4.5, SG No. 2 U-Bend inspections were l

classified as Category C-3.

The initial Row 1 and 2 U-Bend

}

Plus-Point examination samples were 157 tubes.

There were j

three tubes in SG 2 that were determined to be degraded.

I These tubes are located in Row 1.

These tubes were removed from service by plugging.

Since 100 percent of the Row 1 and 2 tubes were examined, no expansion was necessary.

4G 2

TS 4.4.5.5.c also requires a written follow-up report.

TVA plans to provide this information in conjunction with SON's

))0 90-day alternate plugging report.

'7 9905170084 990510 PDR ADOCK 05000328 G

PDR

U.S. Nuclear. Regulatory Commission Page 2' May 10,.1999 4

.Please direct questions concerning this issue to me at (423) 843-7170.or J.

D. Smith at (423) 843-6672.

I Sincerely, A

((((5

Pedro Salas Site Licensing and Industry Affairs. Manager Enclosure cc (Enclosure):

Mr.

R. W. Hernan', Project Manager Nuclear Regulatory Commission

- One White Flint, North 11555 Rockville Pike Rockville, Maryland 20852-2739 NRC Resident Inspector Sequoyah Nuclear Plant 2600 Igou Ferry Road Soddy-Daisy, Tennessee. 37379-3624 Regional Administrator U.S. Nuclear Regulatory Commission Region II-Atlanta Federal Center 61 Forsyth St.,

SW, Suite 23T85 Atlanta, Georgia 30303-3415 i

i k~

l ENCLOSURE STEAM GENERATOR 15-DAY PLUGGING REPORT SEQUOYAH UNIT 2 CYCLE 9 l

SG ROW COL INDICATION 1

1 59 SAI 1

1 76 SAI i

1 4

83 PVN 1

17 37 PVN 1

33 59 40 1

34 53 40 1

36 33 SAI i

l 1

44 34 52 l

l Total Number of Tubes i

l Plugged Thic Generator:

8 l

l SG ROW COL INDICATION 2

1 35 SAI l

2 1

37 SAI 2

1 60 SAI 2

2 20 SAI 2

4 55 SAI 2

8 55 SAI 2

8 77 SCI 2

12 35 SVI l

2 12 71 SAI l

2 22 76 UAI I

2 31 14 47 l

2 32 16 SVI 2

37 21 50 2

40 34 PVN 2

42 31 47 l

2 44 33 41 1

Total Number of Tubes Plugged This Generator:

16 i

1 s

STEAM GENERATOR 15 DAY PLUGGING REPORT SEQUOYAH UNIT 2 CYCLE 9 l

SG ROW COL INDICATION 3

12 40 SCI 3

13 31 SCI 3

13 41 SCI 3

13 61 PVN 3

19 25 SCI 3

22 36 SAI 3

23 23 SAI l

3 31 33 SAI

)

l 3

34 21 SAI 3

38 73 40 Total Number of Tubes Plugged This Generator:

10 l

SG ROW COL INDICATION 4

12 64 SAI I

4 31 15 59 4

44 61 41 Total Number of Tubes 1

Plugged This Generator:

3 J

Total Number of Tubes Plugged This Unit:

37 SAI = Single Axial Indication SCI = Single Circumferential Indication SVI = Single Volumetric Indication PVN = Permeability Variation

  1. indicated the percent through wall