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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217M4461999-10-20020 October 1999 Forwards Rev 8 to Sequoyah Nuclear Plant Physical Security/ Contingency Plan, IAW 10CFR50.54(p).Encl Withheld,Per 10CFR73.21 ML20217J4151999-10-15015 October 1999 Forwards Request for Addl Info Re Util 990624 Application for Amend of TSs That Would Revise TS for Weighing of Ice Condenser Ice Baskets 05000327/LER-1999-002, Forwards LER 99-002-00 Re Start of Units 1 & 2 EDGs as Result of Cable Being Damaged During Installation of Thermo- Lag for Kaowool Upgrade Project1999-10-15015 October 1999 Forwards LER 99-002-00 Re Start of Units 1 & 2 EDGs as Result of Cable Being Damaged During Installation of Thermo- Lag for Kaowool Upgrade Project ML20217G1141999-10-0707 October 1999 Responds to from P Salas,Providing Response to NRC Risk Determination Associated with 990630 Flooding Event at Sequoyah Facility.Meeting to Discuss Risk Determination Issues Scheduled for 991021 in Atlanta,Ga ML20217B2981999-10-0606 October 1999 Discusses Closeout of GL 92-01,rev 1,suppl 1, Reactor Vessel Integrity, for Sequoyah Nuclear Plant,Units 1 & 2. NRC Also Hereby Solicits Any Written Comments That TVA May Have on Current Rvid Data by 991101 ML20217B8431999-10-0505 October 1999 Requests NRC Review & Approval of ASME Code Relief Requests That Were Identified in Plant Second 10-yr ISI Interval for Both Units.Encl 3 Provides Util Procedure for Calculation of ASME Code Coverage for Section XI Nondestructive Exams IR 05000327/19990041999-10-0101 October 1999 Ack Receipt of Providing Comments on Insp Repts 50-327/99-04 & 50-328/99-04.NRC Considered Comments for Apparent Violation Involving 10CFR50.59 Issue ML20217C7101999-10-0101 October 1999 Forwards Response to NRC 990910 RAI Re Sequoyah Nuclear Plant,Units 1 & 2 URI 50-327/98-04-02 & 50-328/98-04-02 Re Ice Weight Representative Sample ML20212J5981999-10-0101 October 1999 Forwards SE Accepting Request for Relief from ASME Boiler & Pressure Vessel Code,Section Xi,Requirements for Certain Inservice Insp at Plnat,Unit 1 ML20212M1081999-09-29029 September 1999 Confirms Intent to Meet with Utils on 991025 in Atlanta,Ga to Discuss Pilot Plants,Shearon Harris & Sequoyah Any Observations & Lessons Learned & Recommendations Re Implementation of Pilot Program ML20217A9451999-09-27027 September 1999 Forwards Insp Repts 50-327/99-05 & 50-328/99-05 on 990718- 0828.One Violation Identified & Being Treated as Non-Cited Violation ML20216J9351999-09-27027 September 1999 Responds to NRC Re Violations Noted in Insp Repts 50-327/99-04 & 50-328/99-04.Corrective Actions:Risk Determination Evaluation Was Performed & Licensee Concluded That Event Is in Green Regulatory Response Band ML20212F0751999-09-23023 September 1999 Forwards SER Granting Util 981021 Request for Relief from ASME Code,Section XI Requirements from Certain Inservice Insp at Sequoyah Nuclear Power Plant,Units 1 & 2 Pursuant to 10CFR50.55a(a)(3)(ii) ML20212F4501999-09-23023 September 1999 Forwards Amends 246 & 237 to Licenses DPR-77 & DPR-79, Respectively & Ser.Amends Approve Request to Revise TSs to Allow Use of Fully Qualified & Tested Spare Inverter in Place of Any of Eight Required Inverters ML20212M1911999-09-21021 September 1999 Discusses Exercise of Enforcement Discretion Re Apparent Violation Noted in Insp Repts 50-327/99-04 & 50-328/99-04 Associated with Implementation of Procedural Changes Which Resulted in Three Containment Penetrations Being Left Open ML20211Q0311999-09-10010 September 1999 Requests Written Documentation from TVA to Provide Technical Assistance to Region II Re TS Compliance & Ice Condenser Maint Practices at Plant ML20216F5441999-09-0707 September 1999 Provides Results of Risk Evaluation of 990630,flooding Event at Sequoyah 1 & 2 Reactor Facilities.Event Was Documented in Insp Rept 50-327/99-04 & 50-328/99-04 & Transmitted in Ltr, ML20211N5681999-09-0101 September 1999 Submits Clarification of Two Issues Raised in Insp Repts 50-327/99-04 & 50-328/99-04,dtd 990813,which Was First Insp Rept Issued for Plant Under NRC Power Reactor Oversight Process Pilot Plant Study ML20211G5881999-08-27027 August 1999 Submits Summary of 990820 Management Meeting Re Plant Performance.List of Attendees & Matl Used in Presentation Enclosed ML20211F8891999-08-25025 August 1999 Forwards Sequoyah Nuclear Plant Unit 1 Cycle 9 Refueling Outage, Re Completed SG Activities,Per TSs 4.4.5.5.b & 4.4.5.5.c ML20211A1851999-08-16016 August 1999 Forwards Proprietary TR WCAP-15128 & non-proprietary Rept WCAP-15129 for NRC Review.Repts Are Provided in Advance of TS Change That Is Being Prepared to Support Cycle 10 Rfo. Proprietary TR Withheld,Per 10CFR2.790 ML20210V1471999-08-13013 August 1999 Forwards Insp Repts 50-327/99-04 & 50-328/99-04 on 990601- 0717.One Potentially Safety Significant Issue Identified.On 990630,inadequate Performance of Storm Drain Sys Caused Water from Heavy Rainfall to Backup & Flood Turbine Bldg ML20211A1921999-08-12012 August 1999 Requests Proprietary TR WCAP-15128, Depth-Based SG Tube Repair Criteria for Axial PWSCC at Dented TSP Intersections, Be Withheld from Public Disclosure Per 10CFR2.790 ML20210Q5011999-08-0505 August 1999 Informs That NRC Plans to Administer Gfes of Written Operator Licensing Exam on 991006 at Sequoyah Nuclear Plant. Sample Registration Ltr Encl ML20210L4291999-08-0202 August 1999 Forwards Sequoyah Nuclear Plant Unit 2 Cycle 9 12-Month SG Insp Rept & SG-99-07-009, Sequoyah Unit-2 Cycle 10 Voltage-Based Repair Criteria 90-Day Rept. Repts Submitted IAW TS 4.4.5.5.b & TS 4.4.5.5.c ML20210L1611999-07-30030 July 1999 Forwards Request for Relief RV-4 Re ASME Class 1,2 & 3 Prvs, Per First ten-year Inservice Test Time Interval.Review & Approval of RV-4 Is Requested to Support Unit 1 Cycle 10 Refueling Outage,Scheduled to Start 000213 ML20210G5301999-07-28028 July 1999 Forwards Sequoyah Nuclear Plant Unit 2 ISI Summary Rept That Contains Historical Record of Repairs,Replacement & ISI & Augmented Examinations That Were Performed on ASME Code Class 1 & 2 Components from 971104-990511 ML20211B9661999-07-26026 July 1999 Informs That Sequoyah Nuclear Plant Sewage Treatment Plant, NPDES 0026450 Outfall 112,is in Standby Status.Flow Has Been Diverted from Sys Since Jan 1998 ML20210B2521999-07-14014 July 1999 Confirms 990712 Telcon Between J Smith of Licensee Staff & M Shannon of NRC Re semi-annual Mgt Meeting Schedule for 990820 in Atlanta,Ga to Discuss Recent Sequoyah Nuclear Plant Performance ML20210J1091999-07-10010 July 1999 Submits Suggestions & Concerns Re Y2K & Nuclear Power Plants ML20196K0381999-06-30030 June 1999 Provides Written Confirmation of Completed Commitment for Final Implementation of Thermo-Lag 330-1 Fire Barrier Corrective Actions at Snp,Per GL 92-08 ML20209E4071999-06-30030 June 1999 Forwards Insp Repts 50-327/99-03 & 50-328/99-03 on 990328- 0531.Violations Being Treated as Noncited Violations ML20196J8261999-06-28028 June 1999 Forwards Safety Evaluation Authorizing Request for Relief from ASME Boiler & Pressure Vessel Code,Section XI Requirements for Certain Inservice Inspections at Sequoyah Nuclear Plant,Units 1 & 2 ML20196G7881999-06-22022 June 1999 Informs NRC of Changes That Util Incorporated Into TS Bases Sections & Trm.Encl Provides Revised TS Bases Pages & TRM Affected by Listed Revs ML20196G1801999-06-21021 June 1999 Requests Termination of SRO License SOP-20751-1,for Lf Hardin,Effective 990611.Subject Individual Resigned from Position at TVA ML20195G1821999-06-0808 June 1999 Requests NRC Review & Approval of ASME Code Relief for ISI Program.Encl 1 Provides Relief Request 1-ISI-14 That Includes Two Attachments.Encl 2 Provides Copy of Related ASME Code Page ML20195E9521999-06-0707 June 1999 Requests Relief from Specific Requirements of ASME Section Xi,Subsection IWE of 1992 Edition,1992 Addenda.Util Has Determined That Proposed Alternatives Would Provide Acceptable Level of Quality & Safety ML20195E9311999-05-28028 May 1999 Informs of Planned Insp Activities for Licensee to Have Opportunity to Prepare for Insps & Provide NRC with Feedback on Any Planned Insps Which May Conflict with Plant Activities ML20195B3631999-05-21021 May 1999 Requests Termination of SRO License for Tj Van Huis,Per 10CFR50.74(a).TJ Van Huis Retired from Util,Effective 990514 ML20207A5721999-05-20020 May 1999 Forwards Correction to Previously Issued Amend 163 to License DPR-79 Re SR 4.1.1.1.1.d Inadvertently Omitted from Pp 3/4 1-1 of Unit 2 TS ML20206Q8791999-05-13013 May 1999 Forwards L36 9990415 802, COLR for Sequoyah Nuclear Plant Unit 2,Cycle 10, IAW Plant TS 6.9.1.14.c 05000327/LER-1999-001, Forwards LER 99-001-00 Re Condition That Resulted in Granting of Enforcement Discretion,Per Failure of Centrifugal Charging Pump.Condition Being Reported IAW 10CFR50.73(a)(2)(i)(B) & (a)(2)(iv)1999-05-11011 May 1999 Forwards LER 99-001-00 Re Condition That Resulted in Granting of Enforcement Discretion,Per Failure of Centrifugal Charging Pump.Condition Being Reported IAW 10CFR50.73(a)(2)(i)(B) & (a)(2)(iv) ML20206M9341999-05-10010 May 1999 Forwards Rept of SG Tube Plugging During Unit 2 Cycle 9 Refueling Outage,As Required by TS 4.4.5.5.a.ISI of Unit 2 SG Tubes Was Completed on 990503 ML20206K6271999-05-0606 May 1999 Requests Termination of SRO License for MR Taggart,License SOP-21336 Due to Resignation on 990430 ML20206J2061999-05-0404 May 1999 Requests Relief from Specified ISI Requirements in Section XI of ASME B&PV Code.Tva Requests Approval to Use Wire Type Penetrameters in Lieu of Plaque Type Penetrameters for Performing Radiographic Insps.Specific Relief Request,Encl ML20209J0391999-04-27027 April 1999 Forwards Annual Radioactive Effluent Release Rept, Radiological Impact Assessment Rept & Rev 41 to ODCM, for Period of Jan-Dec 1998 ML20206C6541999-04-23023 April 1999 Forwards Response to NRC 990127 RAI Re GL 96-05 for Sequoyah Nuclear Plant,Units 1 & 2 ML20206C0841999-04-23023 April 1999 Forwards Insp Repts 50-327/99-02 & 50-328/99-02 on 990214-0327.No Violations Noted ML20206B9591999-04-20020 April 1999 Responds to 990417 Request That NRC Exercise Discretion Not to Enforce Compliance with Actions Required in Unit 1 TS 3.1.2.2,3.1.2.4 & 3.5.2 & Documents 990417 Telephone Conversation When NRC Orally Issued NOED ML20205S5891999-04-17017 April 1999 Documents Request for Discretionary Enforcement for Unit 1 TS LCOs 3.1.2.2,3.1.2.4 & 3.5.2 to Support Completion of Repairs & Testing for 1B-B Centrifugal Charging Pump (CCP) 1999-09-07
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217M4461999-10-20020 October 1999 Forwards Rev 8 to Sequoyah Nuclear Plant Physical Security/ Contingency Plan, IAW 10CFR50.54(p).Encl Withheld,Per 10CFR73.21 05000327/LER-1999-002, Forwards LER 99-002-00 Re Start of Units 1 & 2 EDGs as Result of Cable Being Damaged During Installation of Thermo- Lag for Kaowool Upgrade Project1999-10-15015 October 1999 Forwards LER 99-002-00 Re Start of Units 1 & 2 EDGs as Result of Cable Being Damaged During Installation of Thermo- Lag for Kaowool Upgrade Project ML20217B8431999-10-0505 October 1999 Requests NRC Review & Approval of ASME Code Relief Requests That Were Identified in Plant Second 10-yr ISI Interval for Both Units.Encl 3 Provides Util Procedure for Calculation of ASME Code Coverage for Section XI Nondestructive Exams ML20217C7101999-10-0101 October 1999 Forwards Response to NRC 990910 RAI Re Sequoyah Nuclear Plant,Units 1 & 2 URI 50-327/98-04-02 & 50-328/98-04-02 Re Ice Weight Representative Sample ML20216J9351999-09-27027 September 1999 Responds to NRC Re Violations Noted in Insp Repts 50-327/99-04 & 50-328/99-04.Corrective Actions:Risk Determination Evaluation Was Performed & Licensee Concluded That Event Is in Green Regulatory Response Band ML20211N5681999-09-0101 September 1999 Submits Clarification of Two Issues Raised in Insp Repts 50-327/99-04 & 50-328/99-04,dtd 990813,which Was First Insp Rept Issued for Plant Under NRC Power Reactor Oversight Process Pilot Plant Study ML20211F8891999-08-25025 August 1999 Forwards Sequoyah Nuclear Plant Unit 1 Cycle 9 Refueling Outage, Re Completed SG Activities,Per TSs 4.4.5.5.b & 4.4.5.5.c ML20211A1851999-08-16016 August 1999 Forwards Proprietary TR WCAP-15128 & non-proprietary Rept WCAP-15129 for NRC Review.Repts Are Provided in Advance of TS Change That Is Being Prepared to Support Cycle 10 Rfo. Proprietary TR Withheld,Per 10CFR2.790 ML20211A1921999-08-12012 August 1999 Requests Proprietary TR WCAP-15128, Depth-Based SG Tube Repair Criteria for Axial PWSCC at Dented TSP Intersections, Be Withheld from Public Disclosure Per 10CFR2.790 ML20210L4291999-08-0202 August 1999 Forwards Sequoyah Nuclear Plant Unit 2 Cycle 9 12-Month SG Insp Rept & SG-99-07-009, Sequoyah Unit-2 Cycle 10 Voltage-Based Repair Criteria 90-Day Rept. Repts Submitted IAW TS 4.4.5.5.b & TS 4.4.5.5.c ML20210L1611999-07-30030 July 1999 Forwards Request for Relief RV-4 Re ASME Class 1,2 & 3 Prvs, Per First ten-year Inservice Test Time Interval.Review & Approval of RV-4 Is Requested to Support Unit 1 Cycle 10 Refueling Outage,Scheduled to Start 000213 ML20210G5301999-07-28028 July 1999 Forwards Sequoyah Nuclear Plant Unit 2 ISI Summary Rept That Contains Historical Record of Repairs,Replacement & ISI & Augmented Examinations That Were Performed on ASME Code Class 1 & 2 Components from 971104-990511 ML20210J1091999-07-10010 July 1999 Submits Suggestions & Concerns Re Y2K & Nuclear Power Plants ML20196K0381999-06-30030 June 1999 Provides Written Confirmation of Completed Commitment for Final Implementation of Thermo-Lag 330-1 Fire Barrier Corrective Actions at Snp,Per GL 92-08 ML20196G7881999-06-22022 June 1999 Informs NRC of Changes That Util Incorporated Into TS Bases Sections & Trm.Encl Provides Revised TS Bases Pages & TRM Affected by Listed Revs ML20196G1801999-06-21021 June 1999 Requests Termination of SRO License SOP-20751-1,for Lf Hardin,Effective 990611.Subject Individual Resigned from Position at TVA ML20195G1821999-06-0808 June 1999 Requests NRC Review & Approval of ASME Code Relief for ISI Program.Encl 1 Provides Relief Request 1-ISI-14 That Includes Two Attachments.Encl 2 Provides Copy of Related ASME Code Page ML20195E9521999-06-0707 June 1999 Requests Relief from Specific Requirements of ASME Section Xi,Subsection IWE of 1992 Edition,1992 Addenda.Util Has Determined That Proposed Alternatives Would Provide Acceptable Level of Quality & Safety ML20195B3631999-05-21021 May 1999 Requests Termination of SRO License for Tj Van Huis,Per 10CFR50.74(a).TJ Van Huis Retired from Util,Effective 990514 ML20206Q8791999-05-13013 May 1999 Forwards L36 9990415 802, COLR for Sequoyah Nuclear Plant Unit 2,Cycle 10, IAW Plant TS 6.9.1.14.c 05000327/LER-1999-001, Forwards LER 99-001-00 Re Condition That Resulted in Granting of Enforcement Discretion,Per Failure of Centrifugal Charging Pump.Condition Being Reported IAW 10CFR50.73(a)(2)(i)(B) & (a)(2)(iv)1999-05-11011 May 1999 Forwards LER 99-001-00 Re Condition That Resulted in Granting of Enforcement Discretion,Per Failure of Centrifugal Charging Pump.Condition Being Reported IAW 10CFR50.73(a)(2)(i)(B) & (a)(2)(iv) ML20206M9341999-05-10010 May 1999 Forwards Rept of SG Tube Plugging During Unit 2 Cycle 9 Refueling Outage,As Required by TS 4.4.5.5.a.ISI of Unit 2 SG Tubes Was Completed on 990503 ML20206K6271999-05-0606 May 1999 Requests Termination of SRO License for MR Taggart,License SOP-21336 Due to Resignation on 990430 ML20206J2061999-05-0404 May 1999 Requests Relief from Specified ISI Requirements in Section XI of ASME B&PV Code.Tva Requests Approval to Use Wire Type Penetrameters in Lieu of Plaque Type Penetrameters for Performing Radiographic Insps.Specific Relief Request,Encl ML20209J0391999-04-27027 April 1999 Forwards Annual Radioactive Effluent Release Rept, Radiological Impact Assessment Rept & Rev 41 to ODCM, for Period of Jan-Dec 1998 ML20206C6541999-04-23023 April 1999 Forwards Response to NRC 990127 RAI Re GL 96-05 for Sequoyah Nuclear Plant,Units 1 & 2 ML20205S5891999-04-17017 April 1999 Documents Request for Discretionary Enforcement for Unit 1 TS LCOs 3.1.2.2,3.1.2.4 & 3.5.2 to Support Completion of Repairs & Testing for 1B-B Centrifugal Charging Pump (CCP) ML20205B1091999-03-19019 March 1999 Submits Response to NRC Questions Concerning Lead Test Assembly Matl History,Per Request ML20204H0161999-03-19019 March 1999 Resubmits Util 990302 Response to Violations Noted in Insp Repts 50-327/98-11 & 50-328/98-11.Corrective Actions:Lessons Learned from Event Have Been Provided to Operating Crews ML20204E8251999-03-0505 March 1999 Forwards Sequoyah Nuclear Plant,Four Yr Simulator Test Rept for Period Ending 990321, in Accordance with Requirements of 10CFR55.45 ML20207E6851999-03-0202 March 1999 Responds to NRC Re Violations Noted in Insp Repts 50-327/98-11 & 50-328/98-11.Corrective Actions:Lessons Learned from Event Have Been Provided to Operating Crews ML20207J1171999-01-29029 January 1999 Forwards Copy of Final Exercise Rept for Full Participation Ingestion Pathway Exercise of Offsite Radiological Emergency Response Plans site-specific to Sequoyah NPP ML20202A7141999-01-20020 January 1999 Provides Request for Relief for Delaying Repair on Section of ASME Code Class 3 Piping within Essential Raw Cooling Water Sys ML20198S7141998-12-29029 December 1998 Forwards Cycle 10 Voltage-Based Repair Criteria 90-Day Rept, Per GL 95-05.Rept Is Submitted IAW License Condition 2.C.(9)(d) 05000327/LER-1998-004, Forwards LER 98-004-00,providing Details Concerning Inability to Complete Surveillance within Required Time Interval1998-12-21021 December 1998 Forwards LER 98-004-00,providing Details Concerning Inability to Complete Surveillance within Required Time Interval ML20198D5471998-12-14014 December 1998 Requests That License OP-20313-2 for Je Wright,Be Terminated IAW 10CFR50.74(a).Individual Retiring ML20197J5541998-12-10010 December 1998 Forwards Unit 1 Cycle 9 90-Day ISI Summary Rept IAW IWA-6220 & IWA-6230 of ASME Code,Section Xi.Request for Relief Will Be Submitted to NRC Timeframe to Support Second 10-year Insp Interval,Per 10CFR50.55a 05000327/LER-1998-003, Forwards LER 98-003-00 Re Automatic Reactor Trip with FW Isolation & Auxiliary FW Start as Result of Failure of Vital Inverter & Second Inverter Failure.Event Is Being Reported IAW 10CFR50.73(a)(2)(iv)1998-12-0909 December 1998 Forwards LER 98-003-00 Re Automatic Reactor Trip with FW Isolation & Auxiliary FW Start as Result of Failure of Vital Inverter & Second Inverter Failure.Event Is Being Reported IAW 10CFR50.73(a)(2)(iv) ML20196F9841998-11-25025 November 1998 Provides Changes to Calculated Peak Fuel Cladding Temp, Resulting from Recent Changes to Plant ECCS Evaluation Model ML20195H7891998-11-17017 November 1998 Requests NRC Review & Approval of Five ASME Code Relief Requests Identified in Snp Second ten-year ISI Interval for Units 1 & 2 ML20195E4991998-11-12012 November 1998 Forwards Rev 7 to Physical Security/Contingency Plan.Rev Adds Requirement That Security Personnel Will Assess Search Equipment Alarms & Add Definition of Major Maint.Rev Withheld (Ref 10CFR2.790(d)(1)) 05000328/LER-1998-002, Forwards LER 98-002-00 Re Automatic Turbine & Reactor Trip, Resulting from Failure of Sudden Pressure Relay on 'B' Phase Main Transformer1998-11-10010 November 1998 Forwards LER 98-002-00 Re Automatic Turbine & Reactor Trip, Resulting from Failure of Sudden Pressure Relay on 'B' Phase Main Transformer ML20195G5701998-11-10010 November 1998 Documents Util Basis for 981110 Telcon Request for Discretionary Enforcement for Plant TS 3.8.2.1,Action B,For 120-VAC Vital Instrument Power Board 1-IV.Licensee Determined That Inverter Failed Due to Component Failure ML20155J4031998-11-0505 November 1998 Provides Clarification of Topical Rept Associated with Insertion of Limited Number of Lead Test Assemblies Beginning with Unit 2 Operating Cycle 10 Core ML20154R9581998-10-21021 October 1998 Requests Approval of Encl Request for Relief ISI-3 from ASME Code Requirements Re Integrally Welded Attachments of Supports & Restraints for AFW Piping ML20155B1481998-10-21021 October 1998 Informs That as Result of Discussion of Issues Re Recent Events in Ice Condenser Industry,Ice Condenser Mini-Group (Icmg),Decided to Focus Efforts on Review & Potential Rev of Ice condenser-related TS in Order to Clarify Issues ML20154K1581998-10-13013 October 1998 Forwards Rept Re SG Tube Plugging Which Occurred During Unit 1 Cycle 9 Refueling Outage,Per TS 4.4.5.5.a.ISI of Unit 1 SG Was Completed on 980930 ML20154H6191998-10-0808 October 1998 Forwards Rev 0 to Sequoyah Nuclear Plant Unit 1 Cycle 10 COLR, IAW TS 6.9.1.14.c 05000328/LER-1998-001, Forwards LER 98-001-00 Providing Details Re Automatic Turbine & Reactor Trip Due to Failure of Sudden Pressure Relay on 'B' Phase Main Transformer1998-09-28028 September 1998 Forwards LER 98-001-00 Providing Details Re Automatic Turbine & Reactor Trip Due to Failure of Sudden Pressure Relay on 'B' Phase Main Transformer ML20151W4901998-09-0303 September 1998 Responds to NRC Re Violations Noted in Insp Repts 50-327/98-07 & 50-328/98-07.Corrective Actions:Revised Per SQ971279PER to Address Hardware Issues of Hysteresis, Pressure Shift & Abnormal Popping Noise 1999-09-27
[Table view] |
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e Tennessee Valley Authority. Post Offce Box 2000, Soddy Daisy. Tennessee 37379-2000 Masoud Bajestani Site Vee President Sequoyah Nuclear Plant September 1, 1999 Mr. Louis Reyes .
Regional Administrator U.S. Nuclear Regulatory Commission Region II Atlanta Federal Center 61 Forsyth Street, SW, Suite 23T85
' Atlanta, Georgia 30303-3415
Dear Mr. Reyes:
'In the Matter of ) Docket Nos. 50-327 Tennessee Valley Authority ) 328 SEQUOYAH NUCLEAR PLANT (SQN) - NRC INTEGRATED INSPECTION REPORT 50-327, 50-328/99 REPORT CLARIFICATIONS The purpose of this letter is to clarify two issues raised in Inspection Report 99-04, dated August 13, 1999,.which.was the first inspection report issued for SON under the NRC Power Reactor Oversight Process Pilot Plant Study. The issues requ!. ring' clarification relate to the design of the storm drain system and to'a safety evaluation prepared by SQN personnel in 1991 and how that evaluation may ha". impacted NRC's oversight responsibilities.
The ins.*ction report indicates that these issues are undergoing NRC review. The information and perspectives that we are providing should be helpful in your deliberations.
Regarding the first issue, Sequoyah will aggressively correct the Lvulnerability of the storn. drain system to heavy rains.
With respect to the second issue,-fuel movement was ceased immediately when the containment issue was identified ,
l 9909130022 990901 f 'I 'l7 ()
/-
l l~
PDR ADOCK 05000327
- G PM
% . , m.
U.S. Nuclear Regulatory Commission
.Page_2
_, Sep,tember 1, 1999 (the open penetration issue was raised by the senior resident inspector). Our following clarifications are not intended to ,
-minimize our need to take corrective actions in both of these _d areas. Our discussion is only intended to address actual inaccuracies'and the regulatory importance of these issues.
-As a. result of our' discoveries associated with the closure of '
documents related to the storm drain issue, we are performing a review of significant corrective action program documents issued since 1993. The objective of the review is to identify the subset of these documents that should be t,' reviewed for closure adequacy. We are also preparing a technical specification (TS) change to address ice blowing i and sludge lancing when fuel is being moved. These actions will address the safety aspects of the NRC concerns. ;
STORM DRAIN SYSTEM The inspection report raises two regulatory issues which have a relationship to the design of the system: why the system was not incorporated into the Maintenance Rule Program and how we dispositioned deficiencies identified following a July 1994 rain.
Storm Drain System Design The yard drainage is a gravity flow system which carries surface runoff from an area north-northwest of the turbine building (including roof runoffs) around the transformer yard
-to the yard drainage pond. The drainage for the switchyard
'is handled by a separate system. The lowest catch basin inlet elevations are in front of the turbine building railroad bay (TBRB) door. As such, overflow in the system will occur there first.
There are no established documented design bases requirements or'SQN criteria since it is a nonsafety-related system and does not perform any functions that are described in the Final Safety Analysis Report (FSAR). In fact, the FSAR .
states that "all underground drains were assumed clogged and the surface drainage to be full." Typically, TVA power plants were designed and sized to handle rainfall events with maximum intensity and duration expected in 25-year intervals. i I
l
M. .
U.S. Nuclear Regulatory Commission Page.3 September 1, 1999-The' inspection ~ report. states:
The licensee concluded that.the storm drain System
. lacked redundancy in that only 'o ne drain line leads
- away from the catch basins at the entrance to the turbine building railroad bay and that the basins were a t- a ' low point of the storm drain system, with no
~
surface path available ' to carry water away from the turbine building railroad bay. Therefore, the inspectors noted that because of _ the design, when the storm drain system capacity is exceeded, the system will overflow from the low point catch, basins into the turbine building railroad bay.
That statement, while correct, should be balanced with the SQN FSAR, which establishes the regulatory design requirements for the system. These requirements focus on the assurance of accomplishing a safe shutdown rather than
' minimization of events. The FSAR (Section 2.4.3.4, Probable Maximum Flood Flow) recognizes that the TBRB could flood and
-states that evaluations.take into account that the turbine, control, and' auxiliary buildings will be allowed to flood.
Structures housing safety ~related facilities, systems, and equipment are protected from flooding during a local probable maximum flood. If de-FSAR provisions are left out, the reader may infer that the system does not meet its design or
. regulatory requirements.
Additionally, the June 1995 SQN IPEEE also evaluates the worst potential flood including probable maximum precipitation on the total watershed and critical watersheds,
- including seasonal variations and potential consequential dam
-failures. This document acknowledges the FSAR analysis that i turbine, control, and auxiliary buildings will be allowed'to flood. . The IPEEE concludes that SON design meets the design i
' basis flooding requirements of Regulatory Guide 1.59 and l
-applicable sections of the NRC Standard Review Plan. The IPEEE considerations are important-because they provide the regulatory framework to address flooding.
. Maintenance Rule Considerations -
The inspection report. implies that'TVA did not consider the system during the scoping phase.of the Maintenance Rule. The report states:
I ~
Discussions with the licensee's~. Maintenance Rule specialist indicated that the licensee had not considered or evaluated the site storm drain system o
?~.
c , .
U.S. Nuclear Regulatory Commission Page 4-September-1, 1999-during the scoping phase of .nystems to be included under.the Maintenance Rule. The report continues with l ; Contrary to the above, as of June 30, 1999, the licensee had not included the storm drain system within the' scope'of the Maintenance Rule which is a violation of this requirement.
.. i Based on our review of.the records, the system was considered for inclusion in the Maintenance Rule scope. System No. 040, J
" Station Drainage," includes the. yard storm drains. Station I drainage was reviewed for inclusion in the scope of the rule !
, by the. SON Maintenance Rule Expert Panel, multiple times. As l* . indicated by panel meeting minutes, on June 23, 1994 and l
June 25, 1996,'the panel concluded that the probability that this system could cause a scram is too small for consideration and excluded it from the scope of the rule.
Also, our personnel considered industry guidance, for Maintenance Rule scoping, during their assessment. NEI 93-01 states,in part. i l
8.2.1.4 Nonsafety-Related SSCs Whose Failure Prevents Safety-Related SSCs from Fulfilling their Safety-Related Function .}
Will the' failure of nonsafety-re ated SSCs prevent safety-related SSCs from fulfilling their safety-
[ related function? ,
This step requires that each utility investigate the j systems and system interdependencies to determine failure modes of nonsafety-related SSCs tha t will !
directly affect safety-related functions.
As used in this section of the guidelines, the term
'directly' applies to nonsafety-rela ted SSCn:
- Whose failure prevents a safety func. tion fum being fulfilled; or
. * .W hose failure as a support SSC prevents a safety .
function from being fulfilled . . .
. . . The determination of hypothetical failures that could result from system interdependencies but have not previously been experienced is not required.
8.2.1.5 Nonsafety-Related SSCs Whose Failure Causes Srams or Actuates Safety Systems
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U.S. Nuclear Regulatory Commission Page 5 Sep,tember 1, 1999 i
. . . The determination of hypothetical failures that could result from system interdependencies but have not been previously experienced is not required.
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During.the 1994 flooding of the TBRB, that resulted from storm drain' piping blocked by sediment and debris, Unit 1 operation was reduced to 80 percent power as a conservative precaution'to minimize the potential effect of a single component failure. During the 1999 TBRe flooding, no power reduction was.made. Neither of the flooding conditions resulted in any safety-related SSCs from, fulfilling their function and no actual plant level failure occurred which resulted in a sc' ram or safety system actuation. Th6refore, the power reduction was not an automatic trigger for including the drains under the Maintenance Rule as established in NEI 93-01.
On August 24, 1999, our review of the 1999 TBRB flooding condition again-confirmed that the yard drainage system is a i nonsafety-related system and performs no functions that are described in the FSAR. Therefore, based on scoping requirements and guidelines, and reviews of plant industry experience, the storm drain system does not warrant including it in the scope of the Maintenance Rule. Therefore, we believe that our staff gave proper consideration during the scoping phase of the Maintenance Rule. We also consider that their reasoning remains valid today.
Disposition of Corrective Actions Proposed After 1994 Rain .
Storm )
The report states:
Corrective actions to replace the undersized piping of the storm drain system were canceled.
l Based on the review of the 1994 flooding event, the licensee concluded-that the flow configuration of site
. drainage might not be in accordance with the original 1 site design. Corrective actions to address the site '
flow configuration were canceled. l The licensee canceled the above corrective actions on January 6,1999, citing ' insufficient technical merit and/or inadequate economic benefit' . . . .
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. . . Based on the discussions above, the inspectors concluded that the licensee had not taken adequate corrective actions to protect' the 6. 9kv unit boards.
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U.S. . Nuclear Regulatory Commission L Page,6
, Sep,tember 1, 1999 i
.TheLNRC is correct in stating that those proposed corrective measures.were' closed on January 27, 1999, following evaluation by the. Plant Health Committee. However, that
- discussion should be balanced with an argument of the reasons p :(documented in the Master Issue List Cancellation Tracking l -Form) that' guided our personnel in deciding to cancel the proposed actions.
L The additional analysis identified that the 1994 flood l .resulted from blockage of th'e storm drain pipes which lead l_ from the area in front of the TBRB door (approximately 50-60 l percent of the pipe area _was blocked by accumulated debris P and the remaining cross section was almost completely blocked l
, by a ch'emical.sp'ill mat). The spill mat was removed (an
[ opening had to be cut in the drain line to remove the. spill I
L mat) ' and the drainage system was cleaned of debris. To l prevent. recurrence, maintenance actions were implemented to L prevent clogging due to' debris and accountability was
- established for spill mat recovery to prevent mats from
! getting into the drain system and causing blockage. Based on a calculation at that time,-the drainage system would not meet the 25-year storm interval; therefore, other actions i were considered possible.
l Subsequently a rain' event occurred (1.38 inches in 15 minutes) that exceeded-the intensity and duration that the calculation identified as maximum capacity. It also exceeded the storm event of July 11, 1994, that originated the adverse j condition report. No overflow or flooding. occurred. This confirmed that the actions taken had corrected and prevented recurrence of flooding for similar or greater rainfall l
. . events. It also demonstrated that the maximum capacity is l .actually greater than previously calculated and was equivalent to a 25-year storm intensity. Based on this new information, it was concluded that the actual capacity was
. adequate without additional corrective actions.
l 1In conclusion, we gave proper consideration to the storm drain system.during the scoping of the Maintenance Rule, and theLcancellation of the corrective actions in 1999 was rooted in legitimate technical arguments. As the inspection report recognizes, it was the deficient temporary modification to the system that prompted the 1999 flooding, i
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m y.
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'U.S.INuclear Regulatory Commission "Page 7 Sep,tember 1, 1999 l- IMPACT ON NRC OVERSIGHT RESPONSIBILITIES l'
Relative. to open containmerit penet. rations during fuel tmovement,: the inspection report indicates that the failure to ;
obtain NRC' approval of changes may have impacted the NRC's ability to oversee our activities. j We.suggest that this case did not impact, in any way, NRC's oversight responsibilities. The record is clear that in 1991,-.NRC inspectors, NRR reviewers, and NRC management reviewed the exact same condition the NRC is now evaluating
- ( and considered the safety evaluation' adequate for the treatment of containment requirements during ice blowing and sludge lancing.
.The 1999 inspection report states: j During the review of the three TS' containment penetration violation examples, discussed above, the inspectors noted that the licensee had revised surveillance instruction (SI) 2-SI-OPS-088-006.0, Containment Building Ventilation Isolation (18 Month /100 Hours /7 Days), used.co verify the containment closure requirements of TS surveillance 4.9.4. The original procedura1 requirements noted that the containment penetrations were operable if they were elther capped or isolated wich a manual isolation valve during fuel ' movement. Revision 8 of the. procedure, da ted October 5,1997, documented in Section 6.3 (3), that three safety evalua tions 'had been performed and approved to configure the system for use during core alterations.' This procedure step allowed the licensee to consider the open containment penetrations during fuel movement or core alterations, as acceptable, although contrary to TS 3. 9. 4
. requirements. In addition, the inspectors noted that prior to Ithe ' October 5,1997, revision to the SI, the licensee was using the deficiency notice (DN) process in order to keep the containment penetrations open during fu'el movement or core altera tions.
- Acceptability of. the DNs on the open penetrations was ,
tied _ to the three safety evaluations, . . . which had
'been initiated in 1991, 10 CFR 50.59 states that the licensee may make changes '
to the facility and procedures as described in the
. safety. analysis report (FSAR), without prior l Commission approvala unless the proposed change !
involves?a change in'the TS. FSAR Section 15.5.1.2.5, Fuel Handling ' Instructions, states, in part, that fuel
U.S. Nuclear Regulatory Commission Page 8 September 1, 1999 handling instructions are used to ensure safe and orderly refueling opera tions and that these instructions make reference to other system operations documents that specify precautionary steps to assure that the technical specifications are not violated.
Changes were made to SI 2-SI-OPS-088-006.0, a fuel handling instruction, vithout prior Commission approval, that involved a change to the technical specifications, by using the DN process and subsequently a procedural change, both of which did not meet the TS 3.9.4 requirements. The change to the facility and procedures as described in the safety analysis report, without prior Commission approval, that resulted in a change to the technical -
specif.tcations is considered ta be a violation of 10 CFR 50.59 requirements, and is identified as apparent violation AV 50-328/99004-05, Failure to Meet 10 CFR 50.59 Requirements.
The 1999 inspection report acknowledges that NRC had previously reviewed this issue. It states that:
The inspectors noted that the installation and opera tion of the ice blowing piping to the containment penetration and the use of SG sludge lancing equipment penetration were previously discussed in NRC IR 50-327,328/91-23. This IR indica ted tha t, based on
. discussion between Region II and NRR, these two issues were not regulatory safety significant. However, IR 91-23 did not discuss the effect of these conditions on the containment closure TS, nor did it discuss the effect of creating a 10 CFR 50.59 issue with the procedure changes.
We believe that in 1991 the NRC personnel involved did consider containment closure and the effect that approval would have on procedural controls. Inspection Report 91-23, Section 6, states:
. The inspector reviewed TS 3.9. 4.c and questioned the
-licensee as to whether the ice blowing evolutions were .
in compliance with the TS. The licensee stated that a safety evaluation was in place which supported the evolution. The inspectors requested a copy of the evaluation, and on October 23, 1991 the licensee provided the inspectors with a copy of the safety evaluation which was prepared to support. movement of ice into containment during core alteration periods.
Q U.S. Nuclear Regulatory Conmission Page 9 I ,
September.1, 1999 The inspectors reviewed _ the safety evaluation . . . .
i 'The inspectors met with licensee personnel on October y 24 to discuss the safety evaluation and ask questions.
The licensee explained that they concluded that no
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10.CFR 50.59 issue existed due to their conclusion l that the installed piping between the containment penetrations and the additional equipment building I
(which was considered to be an extension of the auxiliary building) were extensions of the containment ~
l and meet the requirements of GDC 16. After the i
meeting the inspectors reviewed the licensee's safety evaluation with NRC management . . . . Discussions R with NRR resulted in a conclusion that the issues had no regulatbry significance. This position was -
discussed between the licensee and the inspector.
We believe that the conclusion in Inspection Report 99-04 is
- inappropriate. The_ opportunity for NRC oversight has not-l been obviated. Instead, NRC and TVA both now agree that using today's compliance standards, the previous conclusion j was incorrect. NRC personnel--contemporaneous with the safety evaluation--agreed with TVA personnel that ice blowing and sludge lancing activities were permitted by TS 3.9.4.c.
Therefore, the reinterpretation of the aforementioned issues )
should not result in the conclusion that TVA impacted NRC's j oversight responsibilities.
To resolve this issue affecting containment penetrations during fuel movement, we are in progress to revise the TSs to allow the penetrations to be open with administrative controls in place.
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f By taking steps to minimize the probability of rainwater l entry into the 6.9-kV unit boards through use of barriers, sealing of the appropriate conduits during the upcoming outages, review of corrective action document closures for ,
extent of condition, and revision of the TSs to address open l penetrations during fuel movement, the safety aspects of the NRC concerns will be addressed.
In summary, we believe that these two issues have raised engaging topics and our views should help in your analysis of how to treat the regulatory importance of such topics in the future. Hopefully these examples will help us fine tune the new NRC oversight process.
. U . S. . Nuclear Regulatory Commission Page 10 September 1, 1999 Ir you have any questions regarding this response, please contact me at extension (423) 843-7001 or Pedro Salas at extension (423) 843-7170.
Sincerely, be Q 6 O-M. Ba' stani e
cc: r. R. W.-Hernan, Project Manager . .
Nuclear Regulatory Commission One White Flint, North 11555 Rockville Pike Rockville, Maryland 20852-2739 NRC Resident Inspector Sequoyah Nuclear Plant 2600 Igou Ferry Road Soddy-Daisy, Tennessee 37379-3624 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D.C. 20555 4