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NPDES Noncompliance Notification:On 890317,100 Gallons of Petroleum Product Discovered in Storm Drain Impoundment Pond.Extensive Investigation of Possible Sources Conducted But None Identified.Sys Monitoring Temporarily IncreasedML20248B846 |
Person / Time |
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Site: |
Perry |
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Issue date: |
03/22/1989 |
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From: |
Kaplan A CLEVELAND ELECTRIC ILLUMINATING CO. |
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To: |
Kausek S OHIO, STATE OF |
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References |
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PY-CEI-OEPA-007, PY-CEI-OEPA-7, NUDOCS 8904110074 |
Download: ML20248B846 (2) |
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[Table view] |
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THE CLEVELAND ELECTRIC ILLUMINATING COMPANY h
P.O. BOX 97 e PERRY, OMIO 44061 5 TELEPHONE (216) 2594737 E AooRESS 10 CENTER ROAD FROM CLEVELAND: 241 1060 Serving The Best Location in the Nation Al Kaplan PERRY NUCLEAR POWER PLANT vlCE 88E510ENT NUCLEAR 080Va .
, 1 March 22, 1989 PY-CEI/0 EPA-0077 L Ms. Sandra Kausek Environmental Scientist Ohio Environmental Protection Agency Northeast District Office 2001 East Aurora Road Twinsburg, Ohio 44087 Perry Nuclear Power Plant Docket No. 50-440 q NPDES Reportable Occurence l
l
Dear Ms. Kausek:
l In accordance with the terms and conditions of our NPDES Permit No.
3IB00016*CD, the purpose of this letter is to provide written notification of a
! reportable occurrence that took place at the Perry Power Plant site. Ohio l Emergency Response and the National Response Center were notified of the event (Ref. National Response Center Incident No. 3850). The following is a summary of the event.
On March 17, 1989, approximately 100 gallons of a petroleum product were discovered in a storm drain impoundment pond in the Northwest corner of the h Perry Plant site. The impoundment. consists of a concrete spillway, overflow pipe, and a steel barrier wall. It was designed to provide a quiescent zone j for runoff water from the plant site during construction as well as a method of g preventing floating material from entering Lake Erie. It is estimated that the y petroleum product entered the impoundment pond between 0830 and 1600 on
[i 3/17/89, and was contained by the barrier wall. The material in the pond was l discovered at approximately 1430 and Samsel Services, Inc. of Cleveland was j contacted immediately to expedite it's removal. Samsel arrived by 1830 on 3/17/89 and final cleanup activities were completed by 1830, 3/18/89. A heavy rainsterm during cleanup activities increased the flow through the system, resulting in a slight visible sheen on Lake Erie in the vicinity of the impoundment discharge. .
Analysis of samples collected from the pond indicate the material is kerosene mixed with a small amount of lubricating oil.
I g904110074 890322 0 pa ADOCK 0500 f*
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I I
OEPA March 22, 1989~ ,
r i PY-CEI/0 EPA-0077 L !
1 An' extensive investigation of all possible sources of.the material has been conducted; however, ncne.have been identified. Monitoring of the system has temporarily been increased from weekly to daily to ensure compliance with approved
. practices and procedures. No' further gitantities have been detected during this -
activity. . l If you have further questions, please contact Ray Zucker at (216) 259-3737.
Very truly ycurs, l
f Al Kapla l Vice President Nuclear Group AK/sc cc: T. Colburn NRC Resident Office NRC Document Control Desk l
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