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Category:NPDES NONCOMPLIANCE NOTIFICATION
MONTHYEARML20211D2401999-08-19019 August 1999 NPDES Noncompliance Notification:On 990817,chlorinated Water Bypassed Permitted Discharge Point & Entered Storm Drain. Caused by Equipment Malfunction.Valve Will Remain Isolated Until Repaired ML20205G0121999-03-29029 March 1999 NPDES Noncompliance Notification:On 990320,sodium Hypochlorite Leaked to Concrete Secondary Containment.Caused by Failed Supply Line.Spilled Matl Was Pumped from Containment Structure to Containers ML20207M1671999-03-11011 March 1999 NPDES Noncompliance Notification:On 990308,exceedance Occurred,During Simultaneous Treatment of Svc Water Sys & Circulating Water Sys.Dechlorination Feed Rate Will Be Increased ML20195D7691998-11-11011 November 1998 NPDES Noncompliance Notification:On 981020,phone Message from Vendor Laboratory Indicating Analysis of 981008 Sample Drawn from Industrial Wastewater Showed Oil & Grease Content Exceeding Limits.Results Listed.State of Oh Will Issue NOV ML20202D1011998-02-0404 February 1998 NPDES Noncompliance Notification:On 980123,trichloroethylene Leak Occurred at Plant Due to Failed Pressure Indicating Gauge.Area Containing Leak Isolated & Emergency Response Vendor Summoned to Provide Qualified Hazardous Matl Team ML20133M2561997-01-14014 January 1997 NPDES Noncompliance Notification:On 960919,results of self- Monitoring Program Conducted Indicated Mercury Concentration Above Allowable Limit.Future Sample Analysis Results Will Receive Preliminary & Final Review Upon Receipt ML20112B9011996-05-17017 May 1996 NPDES Noncompliance Notification:On 960514,unauthorized Discharge of Plant Circulating Water Discharged to Ground Due to Leak in Expansion Joint in Plant Cooling Tower Basin Wall.All Leakage Being Evaluated for Repair ML20097F1341996-02-12012 February 1996 NPDES Noncompliance Notification:On 960205,transformer Oil Release of Less than 5 Gallons Occurred.Caused by Failure of Bushing on Transformer.Sheen Contained in Impoundment Pond on Plant Site ML20096D7901996-01-15015 January 1996 NPDES Noncompliance Notification Re Unauthorized Leak Noted at Approx 2,300 Gallons on 960111.Caused by Leak in Cooling Basin.Leak Will Be Evaluated for Repair During Plant Outage Scheduled to Begin 960127 ML20082B5871995-03-27027 March 1995 NPDES Noncompliance Notification:From 950322 to 23,effluent Limitation for Discharge of Total Residual Chlorine from Outfall 3IB00016004 Exceeded Due to Failed Valve.Valve Isolated & Will Not Be Used Until Repaired ML20082A9801995-03-27027 March 1995 Notification of 950322 & 23 Release of 3,650 Gallons of 0.8% Sodium Hypochlorite.No Injuries Associated W/Release Noted.Because of Prevailing Wind & Water Currents,Dilution & Low Concentration,No Hazards to Human Health Existed ML20078Q3851995-02-13013 February 1995 NPDES Noncompliance Notification:Discharge of Total Residual Chlorine from Outfall 3IB00016004,discharge Tunnel on 950210.Caused by Mispositioned Switch.Anticipated Time Exceedance Expected to Continue ML20044G8121993-05-26026 May 1993 NPDES Noncompliance Notification:Oil Discharged from Plant Outfall 3IB00016004 & on 930408,approx 35 Gallons of Oil Discharged Through Plant Site Storm Drain to Nameless Stream.Detailed Engineering Analysis Being Conducted ML20101F2711992-06-12012 June 1992 NPDES Noncompliance Notification:Cooling Water Additive & Trial for Circulating Water Sys Will Be Conducted for 3-month Period.Chemical Will Be Injected Twice/Day for 1 H Duration.Slimicide Will Be Considered for Permanent Use PY-CEI-NRR-1269, NPDES Noncompliance Notification:On 901102 Dead Birds Found in Facility Cooling Tower Basin.Caused by Impaction of Birds W/Internal Components & Structures.No Corrective Actions Planned1990-11-30030 November 1990 NPDES Noncompliance Notification:On 901102 Dead Birds Found in Facility Cooling Tower Basin.Caused by Impaction of Birds W/Internal Components & Structures.No Corrective Actions Planned ML19324B6881989-10-30030 October 1989 NPDES Noncompliance Notification:On 891025,plant Released Free Available Chlorine at Concentration of 0.2 mg/1.Caused by Svc Water Chlorination Sys Inadvertently Placed in Continuous Addition Mode W/O Dechlorination Sys Operating ML20248D6201989-09-26026 September 1989 NPDES Noncompliance Notification:On 890921,sulfuric Acid Manually Added to Circulating Water Sys at Excessive Rate. Caused by Plant Acid Addition Sys That Normally Performs Function Being Out of Svc for Maint & Lack of Procedure ML20248B8461989-03-22022 March 1989 NPDES Noncompliance Notification:On 890317,100 Gallons of Petroleum Product Discovered in Storm Drain Impoundment Pond.Extensive Investigation of Possible Sources Conducted But None Identified.Sys Monitoring Temporarily Increased ML20236L5871987-11-0202 November 1987 NPDES Noncompliance Notification:On 871007 Regenerate Neutralization Basin Outfall 3IB00013001 Below Min Allowable Limit for Ph During Discharge.Cause May Have Been Improper Setpoint on Low Ph Trip.Responsible Technician Counseled 1999-08-19
[Table view] Category:TEXT-ENVIRONMENTAL REPORTS
MONTHYEARML20211D2401999-08-19019 August 1999 NPDES Noncompliance Notification:On 990817,chlorinated Water Bypassed Permitted Discharge Point & Entered Storm Drain. Caused by Equipment Malfunction.Valve Will Remain Isolated Until Repaired ML20205G0121999-03-29029 March 1999 NPDES Noncompliance Notification:On 990320,sodium Hypochlorite Leaked to Concrete Secondary Containment.Caused by Failed Supply Line.Spilled Matl Was Pumped from Containment Structure to Containers ML20207M1671999-03-11011 March 1999 NPDES Noncompliance Notification:On 990308,exceedance Occurred,During Simultaneous Treatment of Svc Water Sys & Circulating Water Sys.Dechlorination Feed Rate Will Be Increased ML20207L4901999-02-28028 February 1999 Industrial Pretreatment Quarterly Self-Monitoring Results, for Feb 1999, for Pnpp ML20207L4841999-01-31031 January 1999 Industrial Pretreatment Quarterly Self-Monitoring Results, for Jan 1999, for Pnpp ML20207E8091998-12-31031 December 1998 1998 Annual Occupational Exposure Summary Rept for Pnpp, Unit 1 ML20205T4831998-12-31031 December 1998 Pnpp 1998 Annual Environ & Effluent Release Rept ML20207L4731998-12-31031 December 1998 Industrial Pretreatment Quarterly Self-Monitoring Results, for Dec 1998, for Pnpp ML20199F9131998-12-31031 December 1998 NPDES Discharge Monitoring Rept for Dec 1998 for Perry Nuclear Power Plant. with ML20198C1241998-11-30030 November 1998 Industrial Pretreatment Quarterly Self-Monitoring Results for Nov 1998, for Pnpp ML20198B7581998-11-30030 November 1998 NPDES Monthly Rept for Month of Nov 1998.With ML20195D7691998-11-11011 November 1998 NPDES Noncompliance Notification:On 981020,phone Message from Vendor Laboratory Indicating Analysis of 981008 Sample Drawn from Industrial Wastewater Showed Oil & Grease Content Exceeding Limits.Results Listed.State of Oh Will Issue NOV ML20198C0911998-10-31031 October 1998 Industrial Pretreatment Quarterly Self-Monitoring Results for Oct 1998, for Pnpp ML20195E0821998-10-31031 October 1998 NPDES Monthly Rept for Month of Oct 1998.With ML20198C0871998-09-30030 September 1998 Industrial Pretreatment Quarterly Self-Monitoring Results for Sept 1998, for Pnpp ML20154L7831998-09-30030 September 1998 NPDES Discharge Monitoring Rept for Sept 1998 for Perry Nuclear Power Plant. with ML20151V3421998-08-31031 August 1998 NPDES Discharge Monitoring Rept for Aug 1998. with ML20151W2061998-08-31031 August 1998 Industrial Pretreatment Quarterly Self-Monitoring Results for Aug 1998, for Pnpp ML20151W1941998-07-31031 July 1998 Industrial Pretreatment Quarterly Self-Monitoring Results for July 1998, for Pnpp ML20237B5851998-07-31031 July 1998 NPDES Monthly Discharge Monitoring Rept for July 1998 for Perry Nuclear Power Plant B00016, Amend to NPDES Permit 3IB00016*ED Issued to Cleveland Electric Illuminating Co1998-07-17017 July 1998 Amend to NPDES Permit 3IB00016*ED Issued to Cleveland Electric Illuminating Co ML20151W1861998-06-30030 June 1998 Industrial Pretreatment Quarterly Self-Monitoring Results for June 1998, for Pnpp ML20236P5691998-06-30030 June 1998 NPDES Monthly Rept for June 1998 for Perry Nuclear Power Plant ML20249A0071998-05-31031 May 1998 NPDES Monthly Rept Forms for Month of May 1998 ML20249A1991998-05-31031 May 1998 Industrial Pretreatment Quarterly Self-Monitoring Results for May 1998, for Pnpp ML20247J7421998-04-30030 April 1998 NPDES Monthly Rept Forms for Month of Apr 1998 ML20249A1951998-04-30030 April 1998 Industrial Pretreatment Quarterly Self-Monitoring Results for Apr 1998, for Pnpp ML20249A1931998-03-31031 March 1998 Industrial Pretreatment Quarterly Self-Monitoring Results for Mar 1998, for Pnpp ML20217C1611998-03-31031 March 1998 NPDES Monthly Rept for Mar 1998 for Perry Nuclear Power Plant ML20216D4371998-02-28028 February 1998 NPDES Monthly Rept Forms for Month of Feb 1998.No Violations Occurred During Time Period ML20248L5081998-02-28028 February 1998 Quarterly Self-Monitoring Results for Feb 1998, for Perry Nuclear Power Plant ML20202D1011998-02-0404 February 1998 NPDES Noncompliance Notification:On 980123,trichloroethylene Leak Occurred at Plant Due to Failed Pressure Indicating Gauge.Area Containing Leak Isolated & Emergency Response Vendor Summoned to Provide Qualified Hazardous Matl Team ML20248L4981998-01-31031 January 1998 Quarterly Self-Monitoring Results for Jan 1998, for Perry Nuclear Power Plant ML20202F5711998-01-31031 January 1998 NPDES Monthly Monitoring Rept for Jan 1998 for Perry Nuclear Plant ML20198N5301997-12-31031 December 1997 NPDES Monthly Discharge Rept for Dec 1997 for Perry Nuclear Power Plant ML20199F8721997-12-31031 December 1997 State of Oh Water Withdrawal Facility Registration Annual Rept for Pnpp for 1997 ML20248L4911997-12-31031 December 1997 Quarterly Self-Monitoring Results for Dec 1997, for Perry Nuclear Power Plant ML20247A1731997-12-31031 December 1997 Annual Environ & Effluent Release Rept for Jan-Dec 1997 for Perry Nuclear Power Plant,Unit 1 ML20203H5221997-11-30030 November 1997 NPDES Monthly Rept Forms for Nov 1997.No Discharges Occurred During Month ML20203H3391997-11-30030 November 1997 Industrial Pretreatment Quarterly Self-Monitoring Results, for Nov 1997 ML20199A8441997-10-31031 October 1997 NPDES Monthly Discharge Monitoring Rept for Oct 1997 for Perry Nuclear Power Plant ML20203H3241997-10-31031 October 1997 Industrial Pretreatment Quarterly Self-Monitoring Results, for Oct 1997 ML20203H3141997-09-30030 September 1997 Industrial Pretreatment Quarterly Self-Monitoring Results, for Sept 1997 ML20211P9881997-09-30030 September 1997 NPDES Monthly Rept Forms for Month of Sept 1997 ML20210U8291997-08-31031 August 1997 Industrial Pretreatment Quarterly Self-Monitoring Results, for Aug 1997 ML20210J8061997-07-31031 July 1997 NPDES Monthly Rept Forms for Month of Jul 1997 ML20210U8081997-07-31031 July 1997 Industrial Pretreatment Quarterly Self-Monitoring Results, for Jul 1997 ML20141H0921997-06-30030 June 1997 NPDES Monthly Rept for June 1997 for Perry Nuclear Power Plant ML20210U8021997-06-30030 June 1997 Industrial Pretreatment Quarterly Self-Monitoring Results, for June 1997 ML20140C8111997-05-31031 May 1997 Industrial Pretreatment Quarterly Self-Monitoring Results, for May 1997 1999-08-19
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PERRY NUCLEAR POWER PLANT Mail Accress:
10 CENTER ROAD P.O. B0x 97 Michael D. Lyster PERRY, OHIO 44081 PERRY, OHIO 44081 %:e Presi0ent Nutiear (216)259 3737 November 30, 1990
, PY-CE1/NRR-1269 L U.S. Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555 Perry Nuclear Power Plant Docket No. 50-440 Nonroutine Report -
EPP Section 4.1 and 3.4.2 Centlement Attached is a Nonroutine Report for the Perry Nuclear Power Plant, pursuant to Opera *.ing License NPF-58, Attachment B, Environmental Protection Plan, Sections 4.1 and 5.4.2.
If you have.any questions, please feel free to call.
Since b ,
i t : ~s Michael D. Ly ter MDLILKB njc Attachment cc USNRC Project Manager USNRC Resident Office USNRC Region 111 i
9o11010099 901130
(,DR ADOCK o$00.j ,p,,0 Operating Units. I Clewland Electric illuminatin0 Toledo Edison \\
Attachment PY-CEI/NRR-1269 L Page 1 of 2 Nonroutine Report - EPP Sections 4.1 and 5.4.2 On November 2, 1990, the Environmental Monitoring Element was notified of the presence of dead birds in the Unit 1 cooling tower basin. Fifty-four (54) birds vere found during an inspection conducted that afternoon. The species breakdown was as follows:
Species Number Kinglet 45 Vhite crowned sparrov 3 Varbler sp. 2 Black capped chickadee 2
. Vireo 1 Sparrow sp. 1 Total 54 The Perry Nuclear Power Plant was in Cold Shutdown for a Refueling Outage prior to and during this event. The cooling tower basin was drained and had been cleaned on 10/29/90. No lights were on inside the tnver, and no birds were found around the outside of the tower. Veather conditions during the estimated. time of the event included a high pressure system moving in, accompanied by northerly winds and air temperatures in the 40's.
Additional inspections of the Unit I cooling tower basin vere conducted on 11/5/90, 11/6/90, and 11/8/90. The following dead birds were identified as a-result of these inspections.
Species Date' 11/5 11/6 11/8 Number Kinglet 4 Black capped chickadee 1 1 L Sparrov sp. 1 Hourning dove 1 Total 5 2 1 NOTE: No endangered species were identified during any of the inspections referred to in this report.
l The Unit 2 cooling tower basin was cleaned on 11/6/90 and inspected on 11/8/90 to provide comparative information. No dead birds were found during this inspection. The Unit 2 tower is not in operation and no internal vertical supports or baffle plates are installed at this time to serve as obstacles to birds flying into the tover.
,.-o Attachment PY-CEI/NRR-1269 L Page 2 of 2 The cause is believed to be impaction of the birds with internal components and structures of the Unit 1 cooling tover. This unique occurrence is probably associated with fall migration of the birds involved, and the existing plant and weather conditions. A detailed study undertaken at the Davis-Besse Nuclear Power Station documents similar impactions during fall migrations, and correlates them with the occurrence of high pressure systems. In addition, northerly air flows were noted to increase migration of insectivorous birds such as kinglets, which follow different migration paths each year. (Rei'erence Cooling Towers as Obstacles in Bird Migrations, M. Tomme and V. Jackson, Bevling Green State University, 1979).
Although this is an unusual occurrence at the Perry Plant, it is not unusual in industries that utilize tall stacks or towers. No corrective actions are presently planned.
Initial notification of this event was provided to the USNRC Region III office on 11/2/90. Due to the nature of this occurrence, no other agencies were notified.
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