ML20082B587

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NPDES Noncompliance Notification:From 950322 to 23,effluent Limitation for Discharge of Total Residual Chlorine from Outfall 3IB00016004 Exceeded Due to Failed Valve.Valve Isolated & Will Not Be Used Until Repaired
ML20082B587
Person / Time
Site: Perry FirstEnergy icon.png
Issue date: 03/27/1995
From: Shelton D
CENTERIOR ENERGY
To: Underwood M
OHIO, STATE OF
References
NUDOCS 9504050228
Download: ML20082B587 (2)


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GNTERHHt l ENERGY PERRY NUCLEAR POWER PLANT Mait Address: Donald C. Shelton 0

C CENTER ROAD RR , O 10 44081 SENIOR VICE PRESIDENT PERRY OHIO 44081 NUCLEAR l (216) 259-3rs March 27, 1995 PY-CEI/0 EPA-0218L Ohio Environmental Protection Agency Northeast District Office Attention: Marie Undervood 2110 E. Aurora Road Twinsburg, Ohio 44087 Perry Nuclear Power Plant OEPA Permit No. 3IB00016DD Ladies and Gentlemen:

In accordance with Part III, Section 12.c of the Permit, this letter is serving as confirmation of a telephone report of an effluent limitation exceedance made to the State Emergency Response Commission on 3/23/95.

1. The limitation which has been exceeded: The time limit (two hours) for discharge of Total Residual Chlorine (TRC) from outfall 3IB00016004, the discharge tunnel. Free available chlorine was measured at 0.0 ppm at the final discharge point near the end of the event.
2. The extent of the exceedance: A 23.47 hour5.439815e-4 days <br />0.0131 hours <br />7.771164e-5 weeks <br />1.78835e-5 months <br /> discharge of TRC resulting from approximately 2 gpm of 0.8% sodium hypochlorite entering the plant service water system.
3. The cause of the exceedance: A failed valve.
4. The period of exceedance: From approximately 0030 on 3/22/95 to 0002 on 3/23/95.
5. The anticipated time the exceedance is expected to continue: The release was stopped at 0002 on 3/23/95.
6. Steps being taken to reduce, eliminate and/or prevent recurrence of the exceedance: The valve has been isolated and vill not be used until it is repaired. In addition, a Human Performance Enhancement 040034 opeeng componies cmeona Dectre Nrninoting

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PY-CEI/0 EPA-0218L March 27, 1995 Page 2 of 2 System evaluation is being conducted along with a detailed investigation.. The results of both evaluations vill be used to determine specific actions necessary to prevent recurrence.  ;

If you have questions or require additional information, please contact t

Louise Barton at (216) 280-5512. l Very t y yours, .

LKBesc Nf cc NRC Project Manager  !

NRC Resident Inspector l NRC Document Control Desk NRC Region III l i

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