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Category:NPDES NONCOMPLIANCE NOTIFICATION
MONTHYEARML20211D2401999-08-19019 August 1999 NPDES Noncompliance Notification:On 990817,chlorinated Water Bypassed Permitted Discharge Point & Entered Storm Drain. Caused by Equipment Malfunction.Valve Will Remain Isolated Until Repaired ML20205G0121999-03-29029 March 1999 NPDES Noncompliance Notification:On 990320,sodium Hypochlorite Leaked to Concrete Secondary Containment.Caused by Failed Supply Line.Spilled Matl Was Pumped from Containment Structure to Containers ML20207M1671999-03-11011 March 1999 NPDES Noncompliance Notification:On 990308,exceedance Occurred,During Simultaneous Treatment of Svc Water Sys & Circulating Water Sys.Dechlorination Feed Rate Will Be Increased ML20195D7691998-11-11011 November 1998 NPDES Noncompliance Notification:On 981020,phone Message from Vendor Laboratory Indicating Analysis of 981008 Sample Drawn from Industrial Wastewater Showed Oil & Grease Content Exceeding Limits.Results Listed.State of Oh Will Issue NOV ML20202D1011998-02-0404 February 1998 NPDES Noncompliance Notification:On 980123,trichloroethylene Leak Occurred at Plant Due to Failed Pressure Indicating Gauge.Area Containing Leak Isolated & Emergency Response Vendor Summoned to Provide Qualified Hazardous Matl Team ML20133M2561997-01-14014 January 1997 NPDES Noncompliance Notification:On 960919,results of self- Monitoring Program Conducted Indicated Mercury Concentration Above Allowable Limit.Future Sample Analysis Results Will Receive Preliminary & Final Review Upon Receipt ML20112B9011996-05-17017 May 1996 NPDES Noncompliance Notification:On 960514,unauthorized Discharge of Plant Circulating Water Discharged to Ground Due to Leak in Expansion Joint in Plant Cooling Tower Basin Wall.All Leakage Being Evaluated for Repair ML20097F1341996-02-12012 February 1996 NPDES Noncompliance Notification:On 960205,transformer Oil Release of Less than 5 Gallons Occurred.Caused by Failure of Bushing on Transformer.Sheen Contained in Impoundment Pond on Plant Site ML20096D7901996-01-15015 January 1996 NPDES Noncompliance Notification Re Unauthorized Leak Noted at Approx 2,300 Gallons on 960111.Caused by Leak in Cooling Basin.Leak Will Be Evaluated for Repair During Plant Outage Scheduled to Begin 960127 ML20082B5871995-03-27027 March 1995 NPDES Noncompliance Notification:From 950322 to 23,effluent Limitation for Discharge of Total Residual Chlorine from Outfall 3IB00016004 Exceeded Due to Failed Valve.Valve Isolated & Will Not Be Used Until Repaired ML20082A9801995-03-27027 March 1995 Notification of 950322 & 23 Release of 3,650 Gallons of 0.8% Sodium Hypochlorite.No Injuries Associated W/Release Noted.Because of Prevailing Wind & Water Currents,Dilution & Low Concentration,No Hazards to Human Health Existed ML20078Q3851995-02-13013 February 1995 NPDES Noncompliance Notification:Discharge of Total Residual Chlorine from Outfall 3IB00016004,discharge Tunnel on 950210.Caused by Mispositioned Switch.Anticipated Time Exceedance Expected to Continue ML20044G8121993-05-26026 May 1993 NPDES Noncompliance Notification:Oil Discharged from Plant Outfall 3IB00016004 & on 930408,approx 35 Gallons of Oil Discharged Through Plant Site Storm Drain to Nameless Stream.Detailed Engineering Analysis Being Conducted ML20101F2711992-06-12012 June 1992 NPDES Noncompliance Notification:Cooling Water Additive & Trial for Circulating Water Sys Will Be Conducted for 3-month Period.Chemical Will Be Injected Twice/Day for 1 H Duration.Slimicide Will Be Considered for Permanent Use PY-CEI-NRR-1269, NPDES Noncompliance Notification:On 901102 Dead Birds Found in Facility Cooling Tower Basin.Caused by Impaction of Birds W/Internal Components & Structures.No Corrective Actions Planned1990-11-30030 November 1990 NPDES Noncompliance Notification:On 901102 Dead Birds Found in Facility Cooling Tower Basin.Caused by Impaction of Birds W/Internal Components & Structures.No Corrective Actions Planned ML19324B6881989-10-30030 October 1989 NPDES Noncompliance Notification:On 891025,plant Released Free Available Chlorine at Concentration of 0.2 mg/1.Caused by Svc Water Chlorination Sys Inadvertently Placed in Continuous Addition Mode W/O Dechlorination Sys Operating ML20248D6201989-09-26026 September 1989 NPDES Noncompliance Notification:On 890921,sulfuric Acid Manually Added to Circulating Water Sys at Excessive Rate. Caused by Plant Acid Addition Sys That Normally Performs Function Being Out of Svc for Maint & Lack of Procedure ML20248B8461989-03-22022 March 1989 NPDES Noncompliance Notification:On 890317,100 Gallons of Petroleum Product Discovered in Storm Drain Impoundment Pond.Extensive Investigation of Possible Sources Conducted But None Identified.Sys Monitoring Temporarily Increased ML20236L5871987-11-0202 November 1987 NPDES Noncompliance Notification:On 871007 Regenerate Neutralization Basin Outfall 3IB00013001 Below Min Allowable Limit for Ph During Discharge.Cause May Have Been Improper Setpoint on Low Ph Trip.Responsible Technician Counseled 1999-08-19
[Table view] Category:TEXT-ENVIRONMENTAL REPORTS
MONTHYEARML20211D2401999-08-19019 August 1999 NPDES Noncompliance Notification:On 990817,chlorinated Water Bypassed Permitted Discharge Point & Entered Storm Drain. Caused by Equipment Malfunction.Valve Will Remain Isolated Until Repaired ML20205G0121999-03-29029 March 1999 NPDES Noncompliance Notification:On 990320,sodium Hypochlorite Leaked to Concrete Secondary Containment.Caused by Failed Supply Line.Spilled Matl Was Pumped from Containment Structure to Containers ML20207M1671999-03-11011 March 1999 NPDES Noncompliance Notification:On 990308,exceedance Occurred,During Simultaneous Treatment of Svc Water Sys & Circulating Water Sys.Dechlorination Feed Rate Will Be Increased ML20207L4901999-02-28028 February 1999 Industrial Pretreatment Quarterly Self-Monitoring Results, for Feb 1999, for Pnpp ML20207L4841999-01-31031 January 1999 Industrial Pretreatment Quarterly Self-Monitoring Results, for Jan 1999, for Pnpp ML20207E8091998-12-31031 December 1998 1998 Annual Occupational Exposure Summary Rept for Pnpp, Unit 1 ML20205T4831998-12-31031 December 1998 Pnpp 1998 Annual Environ & Effluent Release Rept ML20207L4731998-12-31031 December 1998 Industrial Pretreatment Quarterly Self-Monitoring Results, for Dec 1998, for Pnpp ML20199F9131998-12-31031 December 1998 NPDES Discharge Monitoring Rept for Dec 1998 for Perry Nuclear Power Plant. with ML20198C1241998-11-30030 November 1998 Industrial Pretreatment Quarterly Self-Monitoring Results for Nov 1998, for Pnpp ML20198B7581998-11-30030 November 1998 NPDES Monthly Rept for Month of Nov 1998.With ML20195D7691998-11-11011 November 1998 NPDES Noncompliance Notification:On 981020,phone Message from Vendor Laboratory Indicating Analysis of 981008 Sample Drawn from Industrial Wastewater Showed Oil & Grease Content Exceeding Limits.Results Listed.State of Oh Will Issue NOV ML20198C0911998-10-31031 October 1998 Industrial Pretreatment Quarterly Self-Monitoring Results for Oct 1998, for Pnpp ML20195E0821998-10-31031 October 1998 NPDES Monthly Rept for Month of Oct 1998.With ML20198C0871998-09-30030 September 1998 Industrial Pretreatment Quarterly Self-Monitoring Results for Sept 1998, for Pnpp ML20154L7831998-09-30030 September 1998 NPDES Discharge Monitoring Rept for Sept 1998 for Perry Nuclear Power Plant. with ML20151V3421998-08-31031 August 1998 NPDES Discharge Monitoring Rept for Aug 1998. with ML20151W2061998-08-31031 August 1998 Industrial Pretreatment Quarterly Self-Monitoring Results for Aug 1998, for Pnpp ML20151W1941998-07-31031 July 1998 Industrial Pretreatment Quarterly Self-Monitoring Results for July 1998, for Pnpp ML20237B5851998-07-31031 July 1998 NPDES Monthly Discharge Monitoring Rept for July 1998 for Perry Nuclear Power Plant B00016, Amend to NPDES Permit 3IB00016*ED Issued to Cleveland Electric Illuminating Co1998-07-17017 July 1998 Amend to NPDES Permit 3IB00016*ED Issued to Cleveland Electric Illuminating Co ML20151W1861998-06-30030 June 1998 Industrial Pretreatment Quarterly Self-Monitoring Results for June 1998, for Pnpp ML20236P5691998-06-30030 June 1998 NPDES Monthly Rept for June 1998 for Perry Nuclear Power Plant ML20249A0071998-05-31031 May 1998 NPDES Monthly Rept Forms for Month of May 1998 ML20249A1991998-05-31031 May 1998 Industrial Pretreatment Quarterly Self-Monitoring Results for May 1998, for Pnpp ML20247J7421998-04-30030 April 1998 NPDES Monthly Rept Forms for Month of Apr 1998 ML20249A1951998-04-30030 April 1998 Industrial Pretreatment Quarterly Self-Monitoring Results for Apr 1998, for Pnpp ML20249A1931998-03-31031 March 1998 Industrial Pretreatment Quarterly Self-Monitoring Results for Mar 1998, for Pnpp ML20217C1611998-03-31031 March 1998 NPDES Monthly Rept for Mar 1998 for Perry Nuclear Power Plant ML20216D4371998-02-28028 February 1998 NPDES Monthly Rept Forms for Month of Feb 1998.No Violations Occurred During Time Period ML20248L5081998-02-28028 February 1998 Quarterly Self-Monitoring Results for Feb 1998, for Perry Nuclear Power Plant ML20202D1011998-02-0404 February 1998 NPDES Noncompliance Notification:On 980123,trichloroethylene Leak Occurred at Plant Due to Failed Pressure Indicating Gauge.Area Containing Leak Isolated & Emergency Response Vendor Summoned to Provide Qualified Hazardous Matl Team ML20248L4981998-01-31031 January 1998 Quarterly Self-Monitoring Results for Jan 1998, for Perry Nuclear Power Plant ML20202F5711998-01-31031 January 1998 NPDES Monthly Monitoring Rept for Jan 1998 for Perry Nuclear Plant ML20198N5301997-12-31031 December 1997 NPDES Monthly Discharge Rept for Dec 1997 for Perry Nuclear Power Plant ML20199F8721997-12-31031 December 1997 State of Oh Water Withdrawal Facility Registration Annual Rept for Pnpp for 1997 ML20248L4911997-12-31031 December 1997 Quarterly Self-Monitoring Results for Dec 1997, for Perry Nuclear Power Plant ML20247A1731997-12-31031 December 1997 Annual Environ & Effluent Release Rept for Jan-Dec 1997 for Perry Nuclear Power Plant,Unit 1 ML20203H5221997-11-30030 November 1997 NPDES Monthly Rept Forms for Nov 1997.No Discharges Occurred During Month ML20203H3391997-11-30030 November 1997 Industrial Pretreatment Quarterly Self-Monitoring Results, for Nov 1997 ML20199A8441997-10-31031 October 1997 NPDES Monthly Discharge Monitoring Rept for Oct 1997 for Perry Nuclear Power Plant ML20203H3241997-10-31031 October 1997 Industrial Pretreatment Quarterly Self-Monitoring Results, for Oct 1997 ML20203H3141997-09-30030 September 1997 Industrial Pretreatment Quarterly Self-Monitoring Results, for Sept 1997 ML20211P9881997-09-30030 September 1997 NPDES Monthly Rept Forms for Month of Sept 1997 ML20210U8291997-08-31031 August 1997 Industrial Pretreatment Quarterly Self-Monitoring Results, for Aug 1997 ML20210J8061997-07-31031 July 1997 NPDES Monthly Rept Forms for Month of Jul 1997 ML20210U8081997-07-31031 July 1997 Industrial Pretreatment Quarterly Self-Monitoring Results, for Jul 1997 ML20141H0921997-06-30030 June 1997 NPDES Monthly Rept for June 1997 for Perry Nuclear Power Plant ML20210U8021997-06-30030 June 1997 Industrial Pretreatment Quarterly Self-Monitoring Results, for June 1997 ML20140C8111997-05-31031 May 1997 Industrial Pretreatment Quarterly Self-Monitoring Results, for May 1997 1999-08-19
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THE CLEVELAND ELECTRIC ILLUMINATING COMPANY l l
- .o. sox DF 5 P385 M, opeo 4 east 5 TetsPHONE (rist8063787 5 ADostes10 osWfsA Mo40 I PMoM UltVsLANo 47618e0 5 Totax: setene ANews8m40A. om Payo Al Kaplan , Serving The Best locetion in the Nation l
- "***W PERRY NUCLEAR POWER PLANT l
"# " October 30, 1989 PY-CE1/0 EPA-0091L Mr. Ermelindo Gomes Environmental Engineer I Di*/ision of Water Pollucion Control i Ohio EPA, Northeast District Office !
2110 East Aurora Road i Twinnburg, Ohio 44087
- f Re Noncompliance Notification f
i 7 Dear Mr. Comes i lu accordance with Part 111, paragraph 12.A. of OEPA Permit No. 31800016*CD, this notification is hereby submitted for a reportable event which occurred on !
Oc tober 25, 1989. I Outfall No. Plant Discharge Location Parameter Discharge Limit Date I 31100016004 Perry Discharge Tunnel Free Avail 9 hours1.041667e-4 days <br />0.0025 hours <br />1.488095e-5 weeks <br />3.4245e-6 months <br /> <2 hours 10/25/89 ;
Chlorine l L
Event Description !
The Ferry Plant Discharge Tunnel teleased free available chlorine at an approximate concentration of 0.2 mg/l between the hours of 10:10 AM and 9:35 i PM (approximately 9 hours1.041667e-4 days <br />0.0025 hours <br />1.488095e-5 weeks <br />3.4245e-6 months <br /> of actual discharge occurred during this period) on !
, October 25, 1989. The event occurred because the Service Water Chierination i
. System was inadvertently placed in a continuous addition mode without the Dochlorination System operating. The Service Water Chlorination Systes {
l ;
L rormally injects aedium hypochlorite for a 1/2 hour period twice per day, ;
j' during which time the Dechlorination System is automatically initiated. l 1
The hervice Water Chlorination Systen 4 normally contro11.ed by 2 timers which j set the frequency of sodium hypochlorite addition (every 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />) and the duration of each addition (1/2 hour). During a chlorination period, which l started at- 10:10 AM on October 25, 1989, the Service Water Weir Structure l (upstrese of the Dechlorination System injection point) was sampled at 10:30 AM and had a free available chlorine concentration of 0.45 mg/1. At 10:35 AM it was discovered that the Dechlarination System had failed to start per its automatic function, due to a power ourage. At 10:40 AM the Plant Discharge j Tunnel was easpled and had a free available chlorine concentration of 0.20 -
ag/1. Af ter the sample was taken of the Plant Discharge Tunnel, the !
Dochlorination System was manually started. At 11:00 AM the Plant Discharge Tunnel was re-sampled and no f ree available chlorine was detected. After the t chlorination cycle was confirmed to have been completed, the dechlorination ;
pump was secured. At 11:15 AM the technician was directed to adjust the 8911080012 891030. [
PDR ADOCK 05000440 e b ' I p
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[ . . Mr. E. Comes Octsber 30, 1989
, PY-CE1/0 EPA-0091 L l
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Service Water Chlorination timers to prevent further chlorination cycles until <
the cause of the dochlorination problem could be determined. However, the l timers were mistakenly placed in a position which caused continuous (
chlorination. At 6:00 PM the sodium hypochlorite storage tank was found empty I and was refilled. 1,ater evaluations determined that the tank was empty at l approximately 3:40 PM, based on sodium typochlorite addition rate. At 9:30 PM i the problem was discovered, and immediate actions were taken to manually start !
the Decielorisation system (which was still in a power outage). The timers I were also reset to their normal position so that the chlorination cycle would !
be completed at 10:00 PM. At 9:35 the Plant Discharge Tannel was sampled and )
no free available chlorine was detected. At 10:00 PM the Service Water Weir l Structure was sampled and had a f ree available chlorine concentration of 0.40 ag/1. l The iree available chlorine release through ther plant discharge tunnel was !
stopped at 9:35 PM when the Dechlorination System was confirmed operational. '
'!he release duration was approximately 9 hours1.041667e-4 days <br />0.0025 hours <br />1.488095e-5 weeks <br />3.4245e-6 months <br /> based on the total time minus i the periods when the Dechlorination System was in operation and the sod!ue .(
hypochlorite storage tank was empty. Sample results for free available ;
chlorine of the Discharge Tunnel (0.2 ag/l at 10:40 AM) and the Service Water {
Weir Structure (0.45 mg/l at 10:30 AM and 0.40 mg/l at 10:00 PM) indicate that '
the f ree available chlorine daily concentration limit of 0.5 mg/l was not i exceeded during the event.
t
.;.e cause of this incident was the improper shutdown of the Service Water i Chlorination System. A technician used the wrong procedure. The procedure that was used addressed a study of chlorination doses needed to control sobra j
! oussel infestation. It did not provide direction for shutting down the !
system. The technician had not received training concerning system shttedown '
and did not know another procedure existed for this task. The power outage }
l which prevented the start of the Dechlorination System was also a contributing !
factor, j
To prevent recurrence all applicable technicians and supervisors will receive f On-The-Job and Classroom traininr to further expand system knowledge and i ensure the correct operation, using the proper procedures, of all Chlorination and Dechlorination Systems. In addition, applicable plant procedures will be reviewed and revised to ensure that power outages that will affect the 3
ll operation of the Chlorination or Dochlorination systems are recognized and ,
acted upon to prevent any future recurrence of this event. ,
Please contact me if you have any questions.
Sn r ly, !
- e Al Kaplan Vice President Nuclear Group AKinjc cca Document Control Desk, NRC T. Colburn P. Hiland Region III Mr. R. Retsler (Lake County Emergency Planning Committee)
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