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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217P2061999-10-26026 October 1999 Forwards for First Energy Nuclear Operating Co Insp Rept 50-346/99-17 on 990928-1001.Insp Was Exam of Activities Conducted Under License Re Implementation of Physical Security Program.No Violations Identified ML20217N3851999-10-20020 October 1999 Forwards RAI Re Licensee 990521 Request for License Amend to Allow Irradiated Fuel to Be Stored in Cask Pit at Davis-Besse,Unit 1.Response Requested within 60 Days from Receipt of Ltr ML20217N2321999-10-15015 October 1999 Requests NRC Approval to Use Alternative to Requirements of 10CFR50.55a(f)(4)(ii).Licensee Requests Extension to Specified Schedule for Implementing Updates to IST Program ML20217G9201999-10-14014 October 1999 Discusses Utils Request for Approval of Quality Assurance Program Changes PY-CEI-NRR-2438, Informs That DBNPS & Pnpp Staffs Have Modified or Withdrawn Several of Positions Proposed within Re Request for Approval of Qap.Revised Positions Encl1999-10-14014 October 1999 Informs That DBNPS & Pnpp Staffs Have Modified or Withdrawn Several of Positions Proposed within Re Request for Approval of Qap.Revised Positions Encl ML20217F8371999-10-0808 October 1999 Forwards Insp Rept 50-346/99-10 on 990802-0913.One Violation Occurred Being Treated as NCV ML20217A5641999-09-30030 September 1999 Informs of Completion of mid-cycle PPR of Davis-Besse on 990901.Informs That NRC Plans to Conduct Addl Insps to Address Questions Raised by Issues Re Operator Errors & Failure to Commit to JOG Topical Rept on MOV Verification ML20212L0691999-09-30030 September 1999 Forwards,For Review & Comment,Copy of Preliminary ASP Analysis of Operational Condition Discovered at Unit 1 on 981014,as Reported in LER 346/98-011 ML20216J6701999-09-24024 September 1999 Forwards Post Examination Documentation for Written Operator Initial License Examination Administered at Davis-Besse Nuclear Power Station on 990920.Without Encls ML20212D3501999-09-21021 September 1999 Forward Copy of Final Accident Sequence Precursor Analysis of Operational Event at Plant,Unit 1 on 980624,reported in LER 346/98-006 05000346/LER-1998-001, Forwards Rev 1 for LER 1998-001,which Updates Corrective Actions & Revises Completion Date Re Implementation of Changes to Plant Emergency Operating Procedure.List of Commitments Attached1999-09-0909 September 1999 Forwards Rev 1 for LER 1998-001,which Updates Corrective Actions & Revises Completion Date Re Implementation of Changes to Plant Emergency Operating Procedure.List of Commitments Attached ML20216E5961999-09-0707 September 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs 3/4.3.2.1,safety Features Actuation Sys Instrumentation & Associated Bases 3/4.3.1 & 3/4.3.2,reactor Protection Sys & Safety Sys Instrumentation ML20211P3001999-09-0707 September 1999 Forwards FEMA Transmitting FEMA Evaluation Rept for 990504 Emergency Preparedness Exercise at Davis-Besse Nuclear Power Plant.No Deficiencies Identified.One Area Requiring C/A & Two Planning Issues Identified ML20211K6681999-08-30030 August 1999 Forwards Copies of Certified Personal Qualification Statement - Licensee (NRC Form 398) for Operator Candidates Listed Below.Without Encls ML20211K6611999-08-30030 August 1999 Forwards Copies of Operator License Renewal Applications for Individuals Listed.Operators Have Successfully Completed Appropriate Operator Requalification Training Program at Dbnps.Without Encls ML20211K0951999-08-30030 August 1999 Forwards Request for Addl Info Re Fire & Seismic Analyses of IPEEE for Davis-Besse Nuclear Power Station,Unit 1. Response Requested within 60 Days ML20211H0201999-08-25025 August 1999 Forwards semi-annual FFD Rept for 990101-0630 for DBNPS, Unit 1,IAW 10CFR26.71(d) ML20211D1171999-08-20020 August 1999 Forwards Insp Rept 50-346/99-09 on 990623-0802.Violations Identified & Being Treated as Noncited Violations ML20211G3911999-08-20020 August 1999 Forwards Update to Estimated Info for Licensing Action Requests Through 010930,re Administrative Ltr 99-02, Operating Reactor Licensing Action Estimates PY-CEI-NRR-2411, Informs That Firstenergy Nuclear Operating Co Has Developed Corporate QA Program Manual for Davis-Besse Nuclear Power Station & Perry Nuclear Power Plant,As Discussed on 990318 Between Util & Nrc.Revised USAR Pages,Encl1999-08-19019 August 1999 Informs That Firstenergy Nuclear Operating Co Has Developed Corporate QA Program Manual for Davis-Besse Nuclear Power Station & Perry Nuclear Power Plant,As Discussed on 990318 Between Util & Nrc.Revised USAR Pages,Encl ML20211J9201999-08-13013 August 1999 Urges NRC to Find Funds for Stockpiling Radiation Pills for Residents Living Near Plant ML20211B0161999-08-13013 August 1999 Forwards SE Accepting Evaluation of Second 10-year Interval Inservice Insp Program Request for Relief Numbers RR-A16, RR-A17 & RR-B9 for Plant,Unit 1 ML20210T1061999-08-12012 August 1999 Forwards Preliminary NRC Forms 398 & 396 for Listed Candidates,Per Operator License Exam Scheduled for Week of 990913.Encl Withheld ML20210S6071999-08-11011 August 1999 Provides Final Response to NRC RAI Re GL 98-01, Y2K Readiness of Computer Systems at Npps ML20210P8051999-08-0909 August 1999 Forwards Insp Rept 50-346/99-15 on 990712-16.No Violations Noted.However,Several Deficiencies Were Identified with Implementation of Remp,Which Collectively Indicated Need for Improved Oversight of Program IR 05000346/19980211999-08-0606 August 1999 Refers to NRC Insp Rept 50-346/98-21 Conducted on 980901- 990513 & Forwards Nov.Two Violations Identified Involving Failure to Maintain Design of Valve & Inadequate C/A for Degraded Condition Cited in Encl NOV 05000346/LER-1998-009, Forwards LER 98-009-01,IAW 10CFR50.73(a)(2)(ii)(B). Commitments Made by Util Are Encl1999-08-0606 August 1999 Forwards LER 98-009-01,IAW 10CFR50.73(a)(2)(ii)(B). Commitments Made by Util Are Encl ML20210H6101999-07-30030 July 1999 Informs That Region III Received Rev 21 to Various Portions of Davis-Besse Nuclear Power Station Emergency Plan.Revision Was Submitted Under Provisions of 10CFR50.54(q) in Apr 1999 ML20210H0491999-07-28028 July 1999 Forwards Application for Amend to License NPF-3,revising TS 3/4.7.5.1, Ultimate Heat Sink, to Allow Plant Operation in Modes 1-4 with Water Temp Less than or Equal to 90 F ML20210G5521999-07-28028 July 1999 Provides Addl Response to 980923 OL Licensing Exam Rept 50-346/98-301 Re OL Exam Administered in Aug 1998.Results of Root Cause Investigation & Corrective Actions,Discussed ML20210G3831999-07-27027 July 1999 Forwards Application for Amend to NPF-3,changing TSs 6.4, Training, 6.5.2.8, Audits, 6.10, Record Retention, 6.14, Process Control Program & 6.15, Odcm ML20211P3071999-07-26026 July 1999 Forwards Final Rept for 990504 Biennial Radiological Emergency Preparedness Exercise for David-Besse Power Station.No Deficiencies Identified for Any Jurisdiction During Exercise ML20210G4391999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs 3/4.3.2.1, Safety Features Actuation Sys Instrumentation, & Associated Bases 3/4.3.1 & 3/4.3.2, Reactor Protection Sys & Safety Sys Instrumentation ML20210G7151999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising TSs 3/4.3.3.1, Radiation Monitoring Instrumentation, 3/4.3.3.2, Instrument - Incore Detectors & 3/4.3.3.9, Instrumentation - Waste Gas Sys Oxygen Monitor ML20210G5151999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs for Implementation of 10CFR50,App J,Option B for Type B & C Containment Leakage Rate Testing ML20210G3211999-07-26026 July 1999 Forwards Written OL Exam & Supporting Matl for Exam to Be Administered at DBNPS During Week of 990913.Listed Encls Withheld from Public Disclosure Until After Exam Complete ML20210C4381999-07-20020 July 1999 Forwards Insp Rept 50-346/99-08 on 990513-0622.Unidentified RCS Leak Approached TS Limit of 1 Gallon Per Minute Prior to Recently Completed Maint Outage.Three Violations of NRC Requirements Identified & Being Treated as NCVs ML20209G3681999-07-15015 July 1999 Advises That Info Submitted in & 990519 Affidavit Re Design & Licensing Rept,Davis-Besse,Unit 1 Cask Pit Rack Installation Project,Holtec Intl, HI-981933,marked Proprietary,Will Be Withheld from Public Disclosure ML20207H6401999-07-0909 July 1999 Discusses Closure of TAC MA0540 Re Util Responses to RAI on GL 92-01,rev 1,suppl 1, Rv Structural Integrity. Staff Has Revised Info in Rvid & Releasing It as Rvid Version 2 ML20209D1341999-07-0808 July 1999 Forwards Notice of Withdrawal of Application for Amend to Operating License.Proposed Change Would Have Modified Facility TSs Pertaining to Allowable as-found Pressure Lift Setting Tolerance of Two Pressurizer Code Safety Valves 05000346/LER-1998-012, Forwards LER 98-012-01,which Is Being Submitted to Provide Addl Info Re 981018 Occurrence.Commitment List Attached1999-07-0707 July 1999 Forwards LER 98-012-01,which Is Being Submitted to Provide Addl Info Re 981018 Occurrence.Commitment List Attached ML20209C3981999-07-0101 July 1999 Responds to NRC Re Violations Noted in Insp Rept 50-346/98-21.Corrective Actions:Developed Rev to Boric Acid Control Program & Work Process Guideline on Plant Leakage ML20209B5821999-06-24024 June 1999 Provides Justification for Rev to Completion Date for One of Insp follow-up Items Cited in Insp Rept 50-346/98-03, Designated as Inspector follow-up Item 50-346/97-201-10 ML20196G1251999-06-23023 June 1999 Responds to NRC RAI Re GL 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants ML20196E5321999-06-17017 June 1999 Forwards Addl Info Re Relief Request RR-A16 to Support NRC Approval of Relief Request ML20195K2751999-06-16016 June 1999 Forwards Safety Evaluation Re GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20196A6601999-06-16016 June 1999 Forwards Master Decommissioning Trust Agreements Revised After 1990 for Ohio Edison Co,Cleveland Electric Illuminating Co,Toledo Edison Co & Pennsylvania Power Co Re Bvnps,Units 1 & 2,DBNPS,Unit 1 & Perry Unit 1 ML20195F9071999-06-10010 June 1999 Forwards Application for Amend to NPF-3,changing Tech Specs 3/4.6.4.4, Hydrogen Purge Sys, TS 3/4.6.5.1, Shield Bldg Emergency Ventilation Sys & TS 3/4.7.6.1, Crevs ML20195F8851999-06-0707 June 1999 Withdraws 950929 License Amend Application,Proposing Mod to Allowable as-found Pressure Lift Setting Tolerance of Two Pressurizer Code Safety Valves ML20207G0751999-06-0707 June 1999 Forwards Insp Rept 50-346/99-04 on 990323-0513.Violations Occurred & Being Treated as non-cited Violations,Consistent with App C of Enforcement Policy 1999-09-09
[Table view] Category:ENGINEERING/CONSTRUCTION/CONSULTING FIRM TO NRC
MONTHYEARML19332C6791989-10-27027 October 1989 FOIA Request for Documents Re pre-implementation Audit of Dcrdr of Plant ML20235A1251987-12-16016 December 1987 Forwards Info Re Resource Technical Svcs,Inc,Including Summary of NRC Contract Work,Nrc Form 26 for Three Existing Contracts,Audit Info,Work History & Lists of Expertise Available for Special Insps & of Current Resource Svcs ML20214R1961987-04-14014 April 1987 Forwards EGG-NTA-7330, Conformance to Generic Ltr 83-28, Item 2.2.1 -- Equipment Classification for All Other Safety- Related Components:Davis-Besse, Final Rept.Plant Conforms to Generic Ltr Item ML20214R3401987-03-30030 March 1987 Documents Final Status of Items Identified in Author Ltr (OBEN-46-86) as Requiring Addl Evaluation &/Or Util Action Before Items Considered Closed.Final Status of Confirmatory Items & Summary of Sys Review & Test Program Encl ML20210L0711986-03-0303 March 1986 FOIA Request That 850724 & 1126 Memos Re Facility Event Be Placed in PDR ML20084R6521984-02-24024 February 1984 FOIA Request for Computer Printout from Sept 1980 to Present of Civil Penalty Info on 27 Listed Nuclear Facilities.Sample Format Encl ML19347E3441981-03-13013 March 1981 Updates 810310 Ltr Re Release of security-related Info. Toledo Edison Released Documents to Oh Public Util Commission.Cleveland Electric Illuminating Co Was Not Involved in Furnishing Documents ML19347E3421981-03-10010 March 1981 Informs That Proprietary IE Insp Repts Had Been Received Through Oh Consumer Counsel.Cleveland Electric Illuminating Co Had Been Careless in Releasing Documents.Nrc Should Take Steps to Prevent Future Leaks ML19329D0891976-01-21021 January 1976 Forwards Page 3658A to Be Inserted in 760130 Transcript ML19329D3011976-01-0909 January 1976 Submits Corrections to 751231 & 760105 Transcripts. Certificate of Svc Encl ML19308D7401970-12-15015 December 1970 Forwards Tentative Version of Script for Slide Presentation Being Prepared for Utils Re Facility.Requests Photos to Complete Program.W/O Encl ML19326A9091970-11-0303 November 1970 Ack Receipt of Notice of Hearing Re Facility CP Application. Permission Requested to Make Oral Statement at 701208 Hearing in Port Clinton,Oh Re Type of Cooling Tower Planned for Facility.Certificate of Svc Encl ML19329C4231970-07-24024 July 1970 Forwards Original Signature Page for 700717 Rept, Review of Seismic Design Criteria for Davis-Besse & List of Ref Documents to Replace Last Page of Rept.W/O Signature Page ML19329C4651970-07-17017 July 1970 Forwards 700717 Rept, Review of Seismic Design Criteria for Davis-Besse. Preliminary Rept Dtd 700515 Revised,Based on Discussions at 700519 Meeting W/Util & NRC Re Amends 5-7 to PSAR ML19319C3801970-04-24024 April 1970 Responds to AEC Request for Review of Vols 1,2 & 3 of PSAR Re Foundation Exploration Program.Addl Info Received Since Transmittal of Original Questions & Comments Re Vols 1,2 & 3.Questions from Review of Addl Info Encl ML19329A8741970-04-24024 April 1970 Forwards Original of Util 700422 Ltr Re Filing of Amend 3 to Psar.W/O Encl ML19329C4771969-10-31031 October 1969 Forwards Seismological & Geological Review of Vols 1,2 & 3 of Psar.Partial List of Comments Submitted w/691028 Ltr.Addl Questions May Be Generated in Future ML19329C4681969-10-28028 October 1969 Forwards Seismic Review of Vols 1,2 & 3 of Psar.Review of Geological Features of Site Will Be Completed Shortly. Addl Questions May Be Generated in Future 1989-10-27
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217N2321999-10-15015 October 1999 Requests NRC Approval to Use Alternative to Requirements of 10CFR50.55a(f)(4)(ii).Licensee Requests Extension to Specified Schedule for Implementing Updates to IST Program PY-CEI-NRR-2438, Informs That DBNPS & Pnpp Staffs Have Modified or Withdrawn Several of Positions Proposed within Re Request for Approval of Qap.Revised Positions Encl1999-10-14014 October 1999 Informs That DBNPS & Pnpp Staffs Have Modified or Withdrawn Several of Positions Proposed within Re Request for Approval of Qap.Revised Positions Encl ML20216J6701999-09-24024 September 1999 Forwards Post Examination Documentation for Written Operator Initial License Examination Administered at Davis-Besse Nuclear Power Station on 990920.Without Encls 05000346/LER-1998-001, Forwards Rev 1 for LER 1998-001,which Updates Corrective Actions & Revises Completion Date Re Implementation of Changes to Plant Emergency Operating Procedure.List of Commitments Attached1999-09-0909 September 1999 Forwards Rev 1 for LER 1998-001,which Updates Corrective Actions & Revises Completion Date Re Implementation of Changes to Plant Emergency Operating Procedure.List of Commitments Attached ML20216E5961999-09-0707 September 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs 3/4.3.2.1,safety Features Actuation Sys Instrumentation & Associated Bases 3/4.3.1 & 3/4.3.2,reactor Protection Sys & Safety Sys Instrumentation ML20211K6611999-08-30030 August 1999 Forwards Copies of Operator License Renewal Applications for Individuals Listed.Operators Have Successfully Completed Appropriate Operator Requalification Training Program at Dbnps.Without Encls ML20211K6681999-08-30030 August 1999 Forwards Copies of Certified Personal Qualification Statement - Licensee (NRC Form 398) for Operator Candidates Listed Below.Without Encls ML20211H0201999-08-25025 August 1999 Forwards semi-annual FFD Rept for 990101-0630 for DBNPS, Unit 1,IAW 10CFR26.71(d) ML20211G3911999-08-20020 August 1999 Forwards Update to Estimated Info for Licensing Action Requests Through 010930,re Administrative Ltr 99-02, Operating Reactor Licensing Action Estimates PY-CEI-NRR-2411, Informs That Firstenergy Nuclear Operating Co Has Developed Corporate QA Program Manual for Davis-Besse Nuclear Power Station & Perry Nuclear Power Plant,As Discussed on 990318 Between Util & Nrc.Revised USAR Pages,Encl1999-08-19019 August 1999 Informs That Firstenergy Nuclear Operating Co Has Developed Corporate QA Program Manual for Davis-Besse Nuclear Power Station & Perry Nuclear Power Plant,As Discussed on 990318 Between Util & Nrc.Revised USAR Pages,Encl ML20211J9201999-08-13013 August 1999 Urges NRC to Find Funds for Stockpiling Radiation Pills for Residents Living Near Plant ML20210T1061999-08-12012 August 1999 Forwards Preliminary NRC Forms 398 & 396 for Listed Candidates,Per Operator License Exam Scheduled for Week of 990913.Encl Withheld ML20210S6071999-08-11011 August 1999 Provides Final Response to NRC RAI Re GL 98-01, Y2K Readiness of Computer Systems at Npps 05000346/LER-1998-009, Forwards LER 98-009-01,IAW 10CFR50.73(a)(2)(ii)(B). Commitments Made by Util Are Encl1999-08-0606 August 1999 Forwards LER 98-009-01,IAW 10CFR50.73(a)(2)(ii)(B). Commitments Made by Util Are Encl ML20210G5521999-07-28028 July 1999 Provides Addl Response to 980923 OL Licensing Exam Rept 50-346/98-301 Re OL Exam Administered in Aug 1998.Results of Root Cause Investigation & Corrective Actions,Discussed ML20210H0491999-07-28028 July 1999 Forwards Application for Amend to License NPF-3,revising TS 3/4.7.5.1, Ultimate Heat Sink, to Allow Plant Operation in Modes 1-4 with Water Temp Less than or Equal to 90 F ML20210G3831999-07-27027 July 1999 Forwards Application for Amend to NPF-3,changing TSs 6.4, Training, 6.5.2.8, Audits, 6.10, Record Retention, 6.14, Process Control Program & 6.15, Odcm ML20210G4391999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs 3/4.3.2.1, Safety Features Actuation Sys Instrumentation, & Associated Bases 3/4.3.1 & 3/4.3.2, Reactor Protection Sys & Safety Sys Instrumentation ML20210G7151999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising TSs 3/4.3.3.1, Radiation Monitoring Instrumentation, 3/4.3.3.2, Instrument - Incore Detectors & 3/4.3.3.9, Instrumentation - Waste Gas Sys Oxygen Monitor ML20210G5151999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs for Implementation of 10CFR50,App J,Option B for Type B & C Containment Leakage Rate Testing ML20211P3071999-07-26026 July 1999 Forwards Final Rept for 990504 Biennial Radiological Emergency Preparedness Exercise for David-Besse Power Station.No Deficiencies Identified for Any Jurisdiction During Exercise ML20210G3211999-07-26026 July 1999 Forwards Written OL Exam & Supporting Matl for Exam to Be Administered at DBNPS During Week of 990913.Listed Encls Withheld from Public Disclosure Until After Exam Complete 05000346/LER-1998-012, Forwards LER 98-012-01,which Is Being Submitted to Provide Addl Info Re 981018 Occurrence.Commitment List Attached1999-07-0707 July 1999 Forwards LER 98-012-01,which Is Being Submitted to Provide Addl Info Re 981018 Occurrence.Commitment List Attached ML20209C3981999-07-0101 July 1999 Responds to NRC Re Violations Noted in Insp Rept 50-346/98-21.Corrective Actions:Developed Rev to Boric Acid Control Program & Work Process Guideline on Plant Leakage ML20209B5821999-06-24024 June 1999 Provides Justification for Rev to Completion Date for One of Insp follow-up Items Cited in Insp Rept 50-346/98-03, Designated as Inspector follow-up Item 50-346/97-201-10 ML20196G1251999-06-23023 June 1999 Responds to NRC RAI Re GL 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants ML20196E5321999-06-17017 June 1999 Forwards Addl Info Re Relief Request RR-A16 to Support NRC Approval of Relief Request ML20196A6601999-06-16016 June 1999 Forwards Master Decommissioning Trust Agreements Revised After 1990 for Ohio Edison Co,Cleveland Electric Illuminating Co,Toledo Edison Co & Pennsylvania Power Co Re Bvnps,Units 1 & 2,DBNPS,Unit 1 & Perry Unit 1 ML20195F9071999-06-10010 June 1999 Forwards Application for Amend to NPF-3,changing Tech Specs 3/4.6.4.4, Hydrogen Purge Sys, TS 3/4.6.5.1, Shield Bldg Emergency Ventilation Sys & TS 3/4.7.6.1, Crevs ML20195F8851999-06-0707 June 1999 Withdraws 950929 License Amend Application,Proposing Mod to Allowable as-found Pressure Lift Setting Tolerance of Two Pressurizer Code Safety Valves ML20207F4231999-06-0202 June 1999 Forwards Rev 1 to DBNPS Emergency Preparedness Evaluated Exercise Manual 990504, IAW 10CFR50.4.NRC Evaluated Exercise Has Been Rescheduled for 991208,since NRC Did Not Evaluate 990504 Exercise ML20207E9561999-05-28028 May 1999 Forwards Update to NRC AL 98-03,re Estimated Info for Licensing Activities Through Sept 30,2000 ML20207E2521999-05-28028 May 1999 Forwards Rev 18,App A,Change 1 to Davis-Besse Nuclear Power Station,Unit 1,industrial Security Plan IAW Provisions of 10CFR50.54(p).Encl Withheld,Per 10CFR73.21 ML20207E7801999-05-21021 May 1999 Forwards Application for Amend to License NPF-3,allowing Use of Expanded Spent Fuel Storage Capacity.Proprietary & non- Proprietary Version of Rev 2 to HI-981933 Re Cask Pit Rack Installation Project,Encl.Proprietary Info Withheld ML20206N0231999-05-0606 May 1999 Forwards License Renewal Applications for Davis-Besse Nuclear Power Station,Unit 1 for ML Klein,Cn Steenbergen & CS Strumsky.Without Encls ML20206D2421999-04-28028 April 1999 Forwards Combined Annual Radiological Environ Operating Rept & Radiological Effluent Release Rept for 1998. Rev 11, Change 1 to ODCM & 1998 Radiological Environ Monitoring Program Sample Analysis Results Also Encl PY-CEI-NRR-2382, Forwards 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for FY98 Also Encl1999-04-21021 April 1999 Forwards 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for FY98 Also Encl ML20206B8831999-04-17017 April 1999 Forwards 1634 Repts Re Results of Monitoring Provided to Individuals at Davis-Besse Nuclear Power Station During 1998,per 10CFR20.2206.Without Repts ML20205K5641999-04-0707 April 1999 Forwards Response to NRC 980415 RAI Re GL 96-06, Assurance of Equipment Operability & Ci During Design-Basis Accident Conditions. Rept FAI/98-126, Waterhammer Phenomena in Containment Air Cooler Swss, Encl ML20205K3871999-04-0707 April 1999 Forwards Copy of Application of Ceic,Oec,Ppc & Teco to FERC, Proposing to Transfer Jurisdictional Transmission Facilities of Firstenergy Operating Companies to American Transmission Sys,Inc.With One Oversize Drawing ML20205J1171999-03-29029 March 1999 Forwards Rev 1 to BAW-2325, Response to RAI Re RPV Integrity, Per GL 92-01,Rev 1,Suppl 1, Reactor Vessel Structural Integrity. Rev Includes Corrected Values in Calculations PY-CEI-NRR-2377, Submits Decommissioning Repts for Bvps,Units 1 & 2,Davis- Besse Nuclear Power Station,Unit 1 & Perry Nuclear Power Plant,Unit 1,per 10CFR50.75(f)(1)1999-03-29029 March 1999 Submits Decommissioning Repts for Bvps,Units 1 & 2,Davis- Besse Nuclear Power Station,Unit 1 & Perry Nuclear Power Plant,Unit 1,per 10CFR50.75(f)(1) ML20205F5961999-03-27027 March 1999 Forwards Comments on Preliminary Accident Sequence Percursor (ASP) Analysis of 980624 Operational Event at Dbnps,Unit 1, as Transmitted by NRC Ltr ML20205D4791999-03-26026 March 1999 Forwards Rept Submitting Results of SG Tube ISI Conducted in Apr 1998.Rept Includes Description of Number & Extent of Tubes Inspected,Location & Percent wall-thickness Penetration for Each Indication of Imperfection ML20205L2031999-03-26026 March 1999 Submits Correction to Dose History of Tj Chambers.Dose Records During 1980-1997 Were Incorrectly Recorded Using Wrong Social Security Number.Nrc Form 5 Not Encl ML20205C7371999-03-25025 March 1999 Certifies That Dbnps,Unit 1,plant-referenced Simulator Continues to Meet Requirements of 10CFR55.45(b) for Simulator Facility Consisting Solely of plant-referenced Simulator.Acceptance Test Program & Test Schedule,Encl ML20205E3551999-03-19019 March 1999 Requests That Proposed Changes to TS 6.8.4.d.2 & TS 6.8.4.d.7 Be Withdrawn from LAR Previously Submitted to NRC ML20204J6361999-03-17017 March 1999 Forwards Firstenergy Corp Annual Rept for 1998 & 1999 Internal Cash Flow Projection as Evidence of Util Guarantee of Retrospective Premiums Which May Be Served Against Facilities PY-CEI-NRR-2375, Forwards List That Details Util Insurers,Policy Numbers & Coverage Limits for Two Power Plants,Per Requirements of 10CFR50.54(w)(3) Re Reporting of Property Insurance Coverage1999-03-15015 March 1999 Forwards List That Details Util Insurers,Policy Numbers & Coverage Limits for Two Power Plants,Per Requirements of 10CFR50.54(w)(3) Re Reporting of Property Insurance Coverage ML20204E6821999-03-12012 March 1999 Requests That Listed Changes Be Made to NRC Document Svc List for Davis-Besse Nuclear Power Station,Unit 1 1999-09-09
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/NEA Idaho National Engineering laboratory March 30, 1987 Mr. Albert W. DeAgazio Project Manager, PWR Directorate #6 Division of PWR Licensing B Bethesda, MD 20014 TRANSMITTAL OF FINAL STATUS OF DAVIS-BESSE CONFIRMATORY ITEMS LISTED IN SECTION V 0F INEL REPORT, TECHNICAL EVALUATION OF DAVIS-BESSE NUCLEAR POWER STATION SYSTEM REVIEW AND TEST PROGRAM (SRTP) EGG-NTA-7104 -
Oben-24-87 Ref: (1) NRC Form 189 Revision 5 for Selected Operating Plant Licensee Issues Program (FIN 06022) Project 3, November 12, 1986 (2) Technical Evaluation of the Davis-Besse Nuclear Power Station System Review and Test Program EGG-NTA-7104 (3) C. F. Obenchain ltr to C. McCracken, Oben-46-86, Transmittal of Updated Status of Davis-Besse Confirmatory Items Listed in Section V of INEL Report, Technical Evaluation of Davis-Besse Nuclear Power Station System Review and Test Program (SRTP)
EGG-NTA-7104
Dear Mr. DeAgazio:
In accordance with Ref (1), INEL issued a Technical Evaluation Report (TER) Ref. (2) on the Davis-8 esse SRTP in January 1986. This TER documented 10 confirmatory items requiring review. Reference (3) provided an updated status of the confirmatory items listed in Ref. (2).
The purpose of this letter is to document the final status of the items identified in Ref. (3) as requiring additional evaluation and/or utility action before they should be considered confirmed and closed. A summary of review and evaluation of the Davis-Besse SRTP and the subsequent witnessing of selected system tests is also provided.
870600008s DR 87o33o ADOCK 05000346 PDR EGnG,a . ,ne. P.O. Box 1M Idaho Falls, ID 83415
t Mr. A. W. DeAgazio March 30, 1987 Oben-24-87 Page 2 This transmittal completes the Davis-8 esse Assistance Task (Project 3) of the referenced NRC Form 189.
If you have any questions on this transmittal or if we can be of further assistance at this time, please contact either Louis Valenti at 208-526-9934 or-(FTS) 583-9934; or Stan Bruske at 208-526-9345 or (FTS) 583-9345.
Very truly yours, t h YP C. F. Obenchain, Manager NRR and I&E Support .
SB:ggo
Enclosure:
(1) Final Status of Confirmatory Items (2) Summary of Davis-Besse SRTP cc: iMit Carrington',7.NRC-TAM 89 G. L. Jones, DOE-ID C. Vandenburgh, NRC-Region III J. O. Zane, EG&G Idaho (w/o Enclosure) f T
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Enclosure 1 March 30, 1987 {
Oben-24-87 Page 1 of 2 )
l l
FINAL STATUS OF CONFIRMATORY ITEMS l
j Reference 2 identified four confirmatory items requiring additional evaluation and/or utility action before they were considered confirmed and j
closed. These items were numbered 5, 7, 9 and 10 in Reference 2.
These items in original form are addressed as follows with an account I
, of their final status accompanying each item:
1 5. The Make-up and Purification System and system functions-identified in the IPRC approved SRTP dated December 3, 1985 did not specifically address the function of Letdown Isolation on a 4
Hi Temperature signal to mitigate a letdown line pipe break. The j utility committed to revise the Davis-Besse Updated Safety '
Analysis Report (USAR) to clarify what systems and system functions are assumed to mitigate a letdown line pipe break-discussed in USAR Section 15.4. This action remains to be ;
- confirmed. l l
i Final Status: This item remains not confirmed and closed by this j review until inclusion to the USAR. The cognizant NRC Inspector has reviewed and closed this item.
a
- 7. The Control Rod Drive System and system functions identified in the IPRC approved SRTP dated December 2, 1985 did not specifically address the Reactor Runback to 15% power. Runbacks i
are addressed in the Integrated Control System and system.
functions identified in the IPRC approved SRTP dated November 14, 1985. However the ICS function does not address the runback function as a safety. function. The Main Steam System and system functions identified in the IPRC approved SRTP dated December 3, 1985 did not specifically address the function of the turbine bypass. The utility committed to revise the USAR to update the discussion provided in Section 15.2 on the turbine .;
trip analysis to indicate that the anticipatory reactor trip i system provides the mitigating functions and delete the !
discussion concerning reactor runback and turbine bypass as-mitigating functions. This action remains to be confirmed.
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i Enclosure 1 l
March 30, 1987
. Oben-24-87 j Page 2 of 2 l Final Status: This item remains not confirmed and closed by this I
review until inclusion to the USAR. The cognizant NRC Inspector has reviewed and closed this item.
- 9. Since the SRTP is continuing to develop as the various phases of program activity are initiated, performed, and reviewed, such things as the appropriate SRTP reliance on integrated plant tests to which Toledo Edison has committed, remains to be confirmed.
Final Status: This item, based on the extent of this review is confirmed and closed.
- 10. The review of selected test outlines to ensure that they ,
encompass all system functions required for safe plant operation I and that the systems are tested under anticipated operating conditions still requires evaluation. In addition, the witnessing and evaluating of selected systems tests to determine their adequacy remains an open item due to the lack of approved testing procedures and the lack of testing to date.
Final Status: This item, based on the extent of this review, is l confirmed and closed. I i
FINAL STATUS CONCLUSION I Items 5 and 7 remain not confirmed and closed by this review until inclusion in the USAR. Items 9 and 10 are confirmed and closed based on the extent of this review. The cognizant NRC Reactor Inspector has reviewed and closed items 5 and 7.
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4 Enclosure 2 March 30, 1987 Oben-24-87 Page 1 of 10
SUMMARY
OF DAVIS-8 ESSE SRTP The process of reviewing the Davis-Besse SRTP included:
o Reviewing procedures both in initial development and after final approval.
o Witnessing performance of tests. This included accompanying the Test Leader on walkdowns of the system to be tested, attending test briefings and observing all or most of the test. On occasions we were only able to witness portions of certain tests due to other tests being conducted concurrently, o Observing troubleshooting, repair and/or modification to systems to correct deficiencies noted during testing, or premodification to systems to perform testing.
i o Evaluating test results.
4 Based on our review, it is concluded that the SRTP has in general 4
accomplished its intended purpose. The SRTP management and testing personnel exhibited a dedicated effort to satisfactorily complete all testing on systems listed in the SRTP. Utility personnel were very responsive to all issues and concerns addressed during our review. All conflicting items and/or open issues that were found during our review have been addressed by the SRTP Group. These conflicting items and issues were reviewed and closed by the cognizant NRC Reactor Inspector.
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I Enclosure 2 l March 30, 1987 Oben-24-87 '
Page 2 of 10 t
A total of 15 site visits were made to Davis-Besse beginning in December 1985 and ending in February 1987. On-site attendance was provided for approximately 50% of the time between December 1985 and February 1987.
Additional time was spent at the home office reviewing and evaluating test procedures, test deficiencies and test results. An average of one site i
visit was made each month, with an average length of stay being two weeks. '
, A list of all site visits and their dates is shown in Table 1.
Even though the. testing that was witnessed as part of our review process was satisfactorily completed, some significant deficiencies were noted. These were also reviewed and closed by the cognizant NRC Reactor
- Inspector.
l The following is a description along with comments of some of the significant deficiencies noted during the review:
- 1. 13.8 kV System TP 850.12 Integrated Electrical ~ Test, 13.8 kV BUS B Lockout--On February 10, 1986,- during testing per step 6.2.9.3 a nail was found in place of a roll pin in the control. power handle for Breaker H8BF4.
Finding of the nail was properly documented. A surveillance report was issued by Quality Control with instructions given to j
perform an inspection of all 13.8/4160 Breakers. This inspection i found no discrepancies. A review of all maintenance performed on Breaker HBBF4 through the last 5 years, turned up two possible cases where the nail could have been introduced.
i Comment: Recommend more frequent inspection of breakers with second and third party verification of breaker conditions when any l inspection, maintenance, or internal activity on the breaker
] is performed.
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l Enclosure 2 i March 30, 1987 l
Oben-24-87 I Page 3 of 10 I
- 2. Nitrogen Supply System TP 850.86 Nitrogen System /RCS Valve Leakage Test--This test was performed early in the SRTP program l and indicated numerous deviations from administrative requirements.
- a. Eight signatures / initials were not accounted for,
- b. There was no test briefing documented in the test chronolog.
- c. . Steps were not signed off by Test Leader at the time of performance. l l
- d. Test deficiencies were not written at the time the )
deficiency occurred.
- e. There was an inordinate amount of time between the end of the test on March 3, 1986 and the receipt of the Evaluation of Leak Testing dated June 23, 1986. This evaluation was performed by the outside independent technical group assisting in the Leak Testing.
Items a through d were addressed by the SRTP Group. Item e was addressed through discussion with the SRTP manager. Disposition i of addressed items is satisfactory.
1 Comment: The performance of this test early in the SRTP program alerted this group to improve their testing and reviewing methods.
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Enclosure 2 March 30, 1987 Oben-24-87 Page 4 of 10 Whenever an outside, independent, technical group is involved in testing, a firm control and responsibility should be established over that group to ensure a timaly response is made to any concerns or requests by the test group.
- 3. Aux-Bldg HVAC TP 851.00 AUX-BLOG NON-RAD HVAC (Low Voltage Switchgear Room)
- a. Methodology of measurements was inadequate
- b. Evaluation of Test Results was inadequate.
- c. Methodology and evaluation were addressed and satisfactorily dispositioned by the SRTP Group.
Comment: Careful review of proper test methodology should be -
performed prior to approval and initiation of test.
Evaluation of test results should be performed by those properly qualified to perform such evaluations, with an independent review following the evaluation.
]
- 4. Main Steam System TP 851.55 MSIV Stroke Time--Testing performed ;
between December 15, 1986 and December 21, 1986, MSIV 101 exhibited a closing response time of 5.7 seconds.
This closing response time did not satisfy two of four different sections of Davis-Besse Technical Specifications, where' l
operability and closure time requirements for the MSIV's.are identified (Section 3.6.3.1--Containment Isolation Yalves, I Section 3/4.7.1.5--Main Steam Line Isolation Valves).
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l Enclosure 2 l March 30, 1987 Oben-24-87 :
! Page 5 of 10 l The station has addressed this in a Safety Evaluation (Reference 3) and concluded all MSIV closure times discussed will satisfy all existing Safety Analysis assumptions.
The station has committed to installing an Air Assist System Test and to test this system and observe any response or change in !
MSIV closure time. Testing is to be performed immediately after i high power reactor trip test.
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Comment: We did not witness this Air Assist System Test.
I
- 5. Integrated Control System TP 850.21 ICS Restart Tuning at Power Test--The Reactor tripped at 15%.
Inadequate communication between test personnel and reactor operators allowed for the removal of an ICS component for troubleshooting, thus contributing to the Reactor Trip (Reference 1).
1 Comment: Thorough communications should have been maintained at j all times. There was a test briefing given by the_ Test
- Leader to the reactor operators. The SRTP Group required that a more thorough briefing be administered along with a discussion of any concerns the reactor operators may have on any of the ICS testing. Also a j thorough and constant communication is to be maintained throughout the test. This has been addressed and noted as being performed in subsequent test briefings.
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Enclosure 2 March 30 1987 Oben-24-87 Page 6 of 10
- 6. The Main feedwater, Auxiliary Feedwater and Motor Driven feed Pump systems were covered extensively in our review. Aside from the normal review process, witnessing of major repair work was performed on Main Feed Pump Turbines 1 and 2. This included witnessing of final alignment checks on No. 1 MFP after its repair of bearing failure on January 1, 1987, witnessing of No. 2 MFP front standard bearing inspection, and No. 1 MFP repair on Stub Shaft and Governor Drive Shaft. Below is a list of Test Procedures performed on the Main feed Pumps, Auxiliary feed Pumps, and the Motor Driven Feed Pump. This list represents a majority of the test procedures performed on the Main Feedwater, Aux Feedwater and Motor Driven feed Pump systems. This does not include the periodic test procedures which were conducted on a more frequent interval as opposed to the test procedu'res which were performed only once.
1 TP850.43 Auxiliary Feedwater Valve Logic Verification TP850.45 AFPT Admission Valve Test on Aux. Steam TP850.48 AFPT Admission Valve and Governor Cold Testing TP850.49 Aux. Feedwater System Refueling Test TP850.50 AFPT Overspeed Trip Test and AFPT Governor Low and High Speed Stop Verification.
l TP850.52 AFP System Monthly Test l
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O Enclosure 2 March 30, 1987 Oben-24-87 Page 7 of 10 TP850.53 AFP Train 1-1 Instr. Functional and Calibration Test TP850.60 Main feed Pump Turbine Drain System Test TP850.61 Main Feed Pump and Turbine Control Oil Test TP850.77 MDFP Motor Run-In i
TP850.79 Steam Generator Remote Shutdown Instrumentation- l Calibration TP850.80 AFW Pressure and Valve Test .
l TP850.96 AFW Pump Room Ventilation Test i
l TP850.99 AFW-MS Supply Line Vibration Test !
l TP851.06 Auxiliary Feedwater Pump Train 1-2 Instrumentation Functional and Calibration Test TP851.07 MDFP Monthly Test TP851.32 Feedwater Control Valve Response to Loss of Instrument i
Air l TP851.52 MFPT Casing Drain Capacity Test TP851.54 MFPT Circuitry Test.
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Enclosure 2 March 30, 1987 Oben-24-87 Page 8 of 10 CONCLUSION The successful completion of testing up to this point by Davis-Besse's SRTP group has demonstrated that systems important to safe plant operation are capable of functioning as intended.
1 The review of Davis-Besse's testing over the last 15 months identified a very responsive approach by the SRTP group to all issues and concerns raised. ~This approach enabled the group to become more proficient in their testing and reviewing methods.
As of February 13, 1987 when the last site visit was completed, all testing, with the exceptions noted under confirmatory items, had been satisfactorily completed. The confirmatory items 5 and 7 have been discussed with and considered closed by the cognizant NRC Reactor Inspector
)
(Reference 4). I 1
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Enclosure 2 March 30, 1987 Oben-24-87 Page 9 of 10 TA8LE 1. DAVIS-BESSE SITE VISITS BY INEL PERSONNEL
- 1. December 2 to December 13, 1985
- 2. December 16 to December 27, 1985
- 3. January 19 to January 24, 1986
- 4. January 27 to January 31, 1986
- 5. February 3 to February 14, 1986
- 6. February 24 to March 7, 1986 l
- 7. March 17 to March 31, 1986
- 8. May 5 to May 23, 1986 ,
i
- 9. June 16 to July 2, 1986
- 10. July 21 to August 17, 1986 l
- 11. September 22 to October 3, 1986
- 12. October 20 to October 30, 1986
- 13. November 11 to November 26, 1986
- 14. December 8 to December 24, 1986
- 15. January 18 to February 13, 1987 l
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Enclosure 2 1 March 30, 1987 Oben-24-87 Page 10 of 10 REFERENCES
- 1. Davis-Besse Unit LER 87-001, Jan. 21, 1987, Reactor Trip Due to Feedwater Isolation and Subsequent Overcooling.
- 2. C. F. Obenchain 1tr to C. McCracken, Oben-46-86, Transmittal of Updated Status of Davis-Besse Confirmatory Items Listed in Section V of INEL Report, Technical Evaluation of Davis-Besse Nuclear Power Station System Review and Test Program (SRTP) EGG-NTA-7104.
- 3. J. Williams, Jr. itr to J. G. Keppler dated December 22, 1986 Serial j No. 1-698.
- 4. L. Valenti, personal communication to C. Vandenburgh on March 18, 1987.
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