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Category:CORRESPONDENCE-LETTERS
MONTHYEARDD-99-12, Informs That Time Provided by NRC Regulation within Which Commission May Act to Review DD-99-12 Has Expired.With Certificate of Svc.Served on 9910281999-10-28028 October 1999 Informs That Time Provided by NRC Regulation within Which Commission May Act to Review DD-99-12 Has Expired.With Certificate of Svc.Served on 991028 ML20217N8261999-10-25025 October 1999 Discusses Errata Re 991021 Filing of Northeast Nuclear Energy Co Answer to Request for Hearing & Petition to Intervene ML20217K3161999-10-19019 October 1999 Forwards Amend 195 to License DPR-61 & Safety Evaluation. Amend Deletes Certain TSs Either No Longer Applicable to Permanently Shutdown & Defueled State of Reactor or Duplicate Regulatory Requirements B17901, Submits Statement of Personal Qualification (NRC Form 398) Along with Supporting Certification of Medical Exam by Facility Licensee (NRC from 396) in Support of License Renewal for PM Miner.Encls Withheld,Per 10CFR2.790(a)(6)1999-10-18018 October 1999 Submits Statement of Personal Qualification (NRC Form 398) Along with Supporting Certification of Medical Exam by Facility Licensee (NRC from 396) in Support of License Renewal for PM Miner.Encls Withheld,Per 10CFR2.790(a)(6) B17886, Requests Permission to Utilize Code Case N-623, Deferral of Insps of Shell-to-Flange & Head-to-Flange of Reactor Vessel,Section Xi,Div 1, for Millstone Unit 21999-10-18018 October 1999 Requests Permission to Utilize Code Case N-623, Deferral of Insps of Shell-to-Flange & Head-to-Flange of Reactor Vessel,Section Xi,Div 1, for Millstone Unit 2 05000336/LER-1999-012, Forwards LER 99-012-00,re Unrecoverable CEA Misalignment Entry Into TS 3.0.3 on 990917.Commitments Made by Util Are Encl1999-10-15015 October 1999 Forwards LER 99-012-00,re Unrecoverable CEA Misalignment Entry Into TS 3.0.3 on 990917.Commitments Made by Util Are Encl ML20217G9491999-10-14014 October 1999 Forwards Exemption from Requirements of 1-CFR50,App E, Section IV.F.2.c,re Conduct of full-participation Exercise in Sept 1999,at Plant,Units 1,2 & 3 B17900, Forwards Revised Assumptions Used in Fuel Handling Accident Analysis & Summary of Results.List of Regulatory Commitments Are Listed in Attachment 11999-10-14014 October 1999 Forwards Revised Assumptions Used in Fuel Handling Accident Analysis & Summary of Results.List of Regulatory Commitments Are Listed in Attachment 1 ML20217D9671999-10-12012 October 1999 Forwards Copy of Transcript of Public Meeting Held by NRC Staff & NNECO on 990825 at Waterford,Connecticut on Decommissioning Program for Millstone,Unit 1.Without Encl CY-99-137, Notifies NRC of Intent to Apply Haddam Neck Plant 10CFR50 App B,Qa Program to Activities Related to Development of ISFSI at Haddam1999-10-12012 October 1999 Notifies NRC of Intent to Apply Haddam Neck Plant 10CFR50 App B,Qa Program to Activities Related to Development of ISFSI at Haddam DD-99-11, Informs That Time Provided by NRC Regulation within Which Commission May Act to Review Director'S Decision (DD-99-11) Expired & That Commission Declined Any Review.Decision Became Final Action on 9910041999-10-0808 October 1999 Informs That Time Provided by NRC Regulation within Which Commission May Act to Review Director'S Decision (DD-99-11) Expired & That Commission Declined Any Review.Decision Became Final Action on 991004 ML20217D3011999-10-0707 October 1999 Forwards Request for Addl Info Re Util 990118 Request for Amend to License NPF-49 to Allow full-core Offloads to Spent Fuel Pool During Core Offloads to Spent Fuel Pool During Core Offload Events ML20217P1201999-10-0606 October 1999 Informs NRC of Proposed Acquisition of Parent Holding Company of Central Maine & Requests NRC Concurrence,Based on Threshold Review,That Proposed Acquisition Does Not,In Fact, Constitute Transfer Subject to 10CFR50.80 ML20217F0031999-10-0606 October 1999 Forwards Original Petition to Intervene Being Filed on Behalf of Clients,Connecticut Coalition Against Millstone & Long Island Coalition Against Millstone,Iaw Provisions of 10CFR2.714 B17892, Requests Withdrawal of License Amend Application Re 24-month SG Tube Insp Surveillance Extensions,Submitted in Util 950726 & s to NRC1999-10-0505 October 1999 Requests Withdrawal of License Amend Application Re 24-month SG Tube Insp Surveillance Extensions,Submitted in Util 950726 & s to NRC ML20217B4711999-10-0404 October 1999 Informs That Staff Did Not Identify Any Safety Concerns Re Licensee Proposals to Modify Commitments Made for Action Items 4.2.1,4.2.2,4.5.1 & 4.5.2 of GL 83-28 by Providing Addl Justifications or Safety Bases for Changes ML20212L1261999-10-0404 October 1999 Forwards Viewgraphs Presented by Licensee at 990923 Meeting with Nrc,In Response to Request ML20212L2171999-10-0101 October 1999 Responds to Recent Ltr to President Wj Clinton,Chairman Jackson & Commissioners,Wd Travers & Ferc,Expressing Concerns Re Millstone NPPs & Continued Lack of Emergency Mgt Plan for Eastern Long Island ML20212L2081999-10-0101 October 1999 Responds to Recent Ltrs to President Wj Clinton,Chairman Jackson & Commissioners & Wd Travers,Expressing Concerns Re Millstone NPPs & Continued Lack of Mgt Plan for Eastern Long Island.Nrc Continues to Monitor Plant Performance ML20212L1971999-10-0101 October 1999 Responds to Recent Ltr to Chairman Jackson & Commissioners Expressing Concerns Re Millstone NPPs & Continued Lack of Emergency Mgt Plan for Eastern Long Island.Nrc Continues to Monitor Plant Performance to Ensure Public Health & Safety ML20212L1831999-10-0101 October 1999 Responds to Recent Ltr to Wd Travers Expressing Concerns Re Millstone NPPs & Continued Lack of Emergency Mgt Plan for Eastern Long Island.Nrc Continues to Monitor Performance of Millstone to Ensure Adequate Protection to Public Health ML20212K1241999-10-0101 October 1999 Responds to Recent Ltrs to Chairman Jackson,Commissioners & Wd Travers,Expressing Concern Re Millstone Npps.Nrc Continues to Monitor Performace of Millstone to Ensure That Public Health & Safety,Adequately Protected ML20212J9991999-10-0101 October 1999 Responds to Recent Ltr to President Clinton,H Clinton, Chairman Jackson &/Or Wd Travers Expressing Concern Re Millstone Npps.Nrc Continues to Monitor Performance of Plant to Ensure That Public Health & Safety Adequately Protected ML20212J3051999-10-0101 October 1999 Discusses GL 97-06 Re Degradation of SG Internals,Dtd 971230.GL Requested Each PWR Licensee to Submit Info That Will Enable NRC Staff to Verify Whether PWR SG Internals Comply & Conform to Current Licensing Basis for Facilities ML20212J2451999-10-0101 October 1999 Informs That Util 980807 & 990629 Responses to GL 98-01, Y2K Readiness of Computer Sys at NPPs Acceptable.Nrc Considers Subj GL to Be Closed for Units 2 &3 ML20212J6621999-09-30030 September 1999 Informs of Completion of mid-cycle PPR of Units 2 & 3 on 990916.Identified Several Recent Instances in Which Condition Repts Were Not Initiated,Resulting in Untimely or Inadequate C/As.Historical Listing of Plant Issues Encl ML20217A9271999-09-30030 September 1999 Discusses Investigation Conducted at Millstone Nuclear Power Station by NRC OI Region I on 980319 to Determine If Contract Training Instructor Was Terminated for Raising Concerns About Quality of Training Matls ML20217B3221999-09-30030 September 1999 Refers to Investigation Rept 1-1997-035 Conducted at Millstone Nuclear Power Station by NRC Ofc of Investigation Field Ofc,Region I on 970915 to Determine Whether Former Health Physics Technician Discriminated Against B17887, Requests Exemption from Requirements of 10CFR140.11(a)(4) Which Requires Licensees to Maintain Secondary Financial Protection Beyond Primary Layer1999-09-28028 September 1999 Requests Exemption from Requirements of 10CFR140.11(a)(4) Which Requires Licensees to Maintain Secondary Financial Protection Beyond Primary Layer ML20216J1341999-09-28028 September 1999 Ltr Contract:Task Order 49, Millstone Units 2 & 3 Employee Concerns Program Insp, Under Contract NRC-03-98-021 B17890, Provides Response to GL 99-02, Laboratory Testing of Nuclear-Grade Activated Charcoal1999-09-27027 September 1999 Provides Response to GL 99-02, Laboratory Testing of Nuclear-Grade Activated Charcoal B17883, Forwards Mnps Unit 3 ISI Summary Rept,Cycle 6, IAW ASME Section XI,IWA-62301999-09-27027 September 1999 Forwards Mnps Unit 3 ISI Summary Rept,Cycle 6, IAW ASME Section XI,IWA-6230 B17888, Informs That There No Longer Exists Need to Maintain Millstone Unit 2 SRO License for CA Hines,License SOP-10741-01,effective 9909151999-09-24024 September 1999 Informs That There No Longer Exists Need to Maintain Millstone Unit 2 SRO License for CA Hines,License SOP-10741-01,effective 990915 B17884, Forwards NRC Form 536, Operator Licensing Exam Data, for Mnps,Units 2 & 3,per Administrative Ltr 99-031999-09-24024 September 1999 Forwards NRC Form 536, Operator Licensing Exam Data, for Mnps,Units 2 & 3,per Administrative Ltr 99-03 ML20212D0341999-09-20020 September 1999 Expresses Appreciation for Accepting NRC Request for Tour of Haddam Neck Facility During on 991014.Invites R Mellor to Participate in NRC 1999 Decommissioninng Power Reactor Work- Shop:Nrc Insp Program at Decommissioning Power Reactors ML20212F4961999-09-20020 September 1999 Forwards Insp Repts 50-245/99-08,50-336/99-08 & 50-423/99-08 on 990615-0809.Four Violations of NRC Requirements Occurred & Being Treated as Ncvs,Consistent with App C of Enforcement Policy 05000336/LER-1999-001, Forwards LER 99-001-00 Re Thermal Reactor Power Limit That Was Exceeded.Commitments Made by Util Encl1999-09-20020 September 1999 Forwards LER 99-001-00 Re Thermal Reactor Power Limit That Was Exceeded.Commitments Made by Util Encl B17867, Requests Relief from Requirements of 10CFR50.55a(g),IAW ASME Section XI for Millstone,Unit 3.Util Requests Relief from Performing Visual Exam of Reactor Pressure Supports to Extent Required by Code for Class 1 Supports1999-09-17017 September 1999 Requests Relief from Requirements of 10CFR50.55a(g),IAW ASME Section XI for Millstone,Unit 3.Util Requests Relief from Performing Visual Exam of Reactor Pressure Supports to Extent Required by Code for Class 1 Supports B17865, Provides NRC Staff with Updated Proposed Rev of FSAR Section 14.6.3, Radiological Consequences of SG Tube Failure. Updated Proposed Rev Will Replace Info Provided in Attachment 3 of Initial Submittal1999-09-16016 September 1999 Provides NRC Staff with Updated Proposed Rev of FSAR Section 14.6.3, Radiological Consequences of SG Tube Failure. Updated Proposed Rev Will Replace Info Provided in Attachment 3 of Initial Submittal B17876, Informs That Util Will Adopt Last Approved Northeast Util QA Program (Nuqap) Tr,Rev 21,dtd 990630,as Unit 1 Nuqap,Per Decision to Permanently Cease Operations at Subject Plant1999-09-16016 September 1999 Informs That Util Will Adopt Last Approved Northeast Util QA Program (Nuqap) Tr,Rev 21,dtd 990630,as Unit 1 Nuqap,Per Decision to Permanently Cease Operations at Subject Plant B17880, Forwards NRC Form 398 & NRC Form 396 for Rf Martin,License SOP-10397-0.Encls Withheld Per 10CFR2.790(a)(6)1999-09-15015 September 1999 Forwards NRC Form 398 & NRC Form 396 for Rf Martin,License SOP-10397-0.Encls Withheld Per 10CFR2.790(a)(6) B17881, Forwards NRC Form 398 & NRC Form 396 for Le Olsen,License SOP-10398-2.Encl Withheld Per 10CFR2.790(a)(6)1999-09-15015 September 1999 Forwards NRC Form 398 & NRC Form 396 for Le Olsen,License SOP-10398-2.Encl Withheld Per 10CFR2.790(a)(6) B17859, Forwards up-to-date Distribution Lists for NRC Correspondence to NNECO & NUSCO.Side-bars Indicate Changes from Previous Lists Provided to NRC on 9801281999-09-15015 September 1999 Forwards up-to-date Distribution Lists for NRC Correspondence to NNECO & NUSCO.Side-bars Indicate Changes from Previous Lists Provided to NRC on 980128 B17882, Forwards NRC Forms 398 & 369 in Support of License Renewal for Bb Parrish,License SOP-10399-2.Encl Withheld Per 10CFR2.790(a)(6)1999-09-15015 September 1999 Forwards NRC Forms 398 & 369 in Support of License Renewal for Bb Parrish,License SOP-10399-2.Encl Withheld Per 10CFR2.790(a)(6) B17872, Informs of Election to Consolidate Previous Commitments Re Work Observation Program with Two New Programmatic Commitments Listed in Attachment 11999-09-14014 September 1999 Informs of Election to Consolidate Previous Commitments Re Work Observation Program with Two New Programmatic Commitments Listed in Attachment 1 B17838, Forwards Revs 34 & 35 to Physical Security Plan.Explanation of Changes Provided as Attachment 1.Without Encls1999-09-10010 September 1999 Forwards Revs 34 & 35 to Physical Security Plan.Explanation of Changes Provided as Attachment 1.Without Encls ML20212A9011999-09-10010 September 1999 Forwards Environ Assessment & Finding of No Significant Impact Re Application for Exemption,Dtd 990803.Proposed Exemption Would Provide Relief from Requirement of 10CFR50 ML20212A7501999-09-10010 September 1999 Forwards Staff Requirements Memo Response,Dtd 990525,which Provides Actions NRC Plans for Continued Oversight of safety-conscious Work Environ & Employee Concerns Program ML20212A3171999-09-10010 September 1999 Discusses Investigation Rept 1-1998-045 Conducted on 981112 to Determine If Former Senior Health Physics Technician Being Denied Employment at Millstone in Retaliation for Having Raised Safety Concerns in Past.Synopsis Encl ML20211J9291999-09-0303 September 1999 Forwards mark-ups & Retypes of Proposed Conforming License Changes Required in Connection with Transfers Being Sought in 990615 Application of Montaup Electric Co & New England Power Co for Transfer of Licenses & Ownership Interests 1999-09-30
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217N8261999-10-25025 October 1999 Discusses Errata Re 991021 Filing of Northeast Nuclear Energy Co Answer to Request for Hearing & Petition to Intervene B17901, Submits Statement of Personal Qualification (NRC Form 398) Along with Supporting Certification of Medical Exam by Facility Licensee (NRC from 396) in Support of License Renewal for PM Miner.Encls Withheld,Per 10CFR2.790(a)(6)1999-10-18018 October 1999 Submits Statement of Personal Qualification (NRC Form 398) Along with Supporting Certification of Medical Exam by Facility Licensee (NRC from 396) in Support of License Renewal for PM Miner.Encls Withheld,Per 10CFR2.790(a)(6) B17886, Requests Permission to Utilize Code Case N-623, Deferral of Insps of Shell-to-Flange & Head-to-Flange of Reactor Vessel,Section Xi,Div 1, for Millstone Unit 21999-10-18018 October 1999 Requests Permission to Utilize Code Case N-623, Deferral of Insps of Shell-to-Flange & Head-to-Flange of Reactor Vessel,Section Xi,Div 1, for Millstone Unit 2 05000336/LER-1999-012, Forwards LER 99-012-00,re Unrecoverable CEA Misalignment Entry Into TS 3.0.3 on 990917.Commitments Made by Util Are Encl1999-10-15015 October 1999 Forwards LER 99-012-00,re Unrecoverable CEA Misalignment Entry Into TS 3.0.3 on 990917.Commitments Made by Util Are Encl B17900, Forwards Revised Assumptions Used in Fuel Handling Accident Analysis & Summary of Results.List of Regulatory Commitments Are Listed in Attachment 11999-10-14014 October 1999 Forwards Revised Assumptions Used in Fuel Handling Accident Analysis & Summary of Results.List of Regulatory Commitments Are Listed in Attachment 1 CY-99-137, Notifies NRC of Intent to Apply Haddam Neck Plant 10CFR50 App B,Qa Program to Activities Related to Development of ISFSI at Haddam1999-10-12012 October 1999 Notifies NRC of Intent to Apply Haddam Neck Plant 10CFR50 App B,Qa Program to Activities Related to Development of ISFSI at Haddam ML20217P1201999-10-0606 October 1999 Informs NRC of Proposed Acquisition of Parent Holding Company of Central Maine & Requests NRC Concurrence,Based on Threshold Review,That Proposed Acquisition Does Not,In Fact, Constitute Transfer Subject to 10CFR50.80 ML20217F0031999-10-0606 October 1999 Forwards Original Petition to Intervene Being Filed on Behalf of Clients,Connecticut Coalition Against Millstone & Long Island Coalition Against Millstone,Iaw Provisions of 10CFR2.714 B17892, Requests Withdrawal of License Amend Application Re 24-month SG Tube Insp Surveillance Extensions,Submitted in Util 950726 & s to NRC1999-10-0505 October 1999 Requests Withdrawal of License Amend Application Re 24-month SG Tube Insp Surveillance Extensions,Submitted in Util 950726 & s to NRC B17887, Requests Exemption from Requirements of 10CFR140.11(a)(4) Which Requires Licensees to Maintain Secondary Financial Protection Beyond Primary Layer1999-09-28028 September 1999 Requests Exemption from Requirements of 10CFR140.11(a)(4) Which Requires Licensees to Maintain Secondary Financial Protection Beyond Primary Layer B17890, Provides Response to GL 99-02, Laboratory Testing of Nuclear-Grade Activated Charcoal1999-09-27027 September 1999 Provides Response to GL 99-02, Laboratory Testing of Nuclear-Grade Activated Charcoal B17883, Forwards Mnps Unit 3 ISI Summary Rept,Cycle 6, IAW ASME Section XI,IWA-62301999-09-27027 September 1999 Forwards Mnps Unit 3 ISI Summary Rept,Cycle 6, IAW ASME Section XI,IWA-6230 B17884, Forwards NRC Form 536, Operator Licensing Exam Data, for Mnps,Units 2 & 3,per Administrative Ltr 99-031999-09-24024 September 1999 Forwards NRC Form 536, Operator Licensing Exam Data, for Mnps,Units 2 & 3,per Administrative Ltr 99-03 B17888, Informs That There No Longer Exists Need to Maintain Millstone Unit 2 SRO License for CA Hines,License SOP-10741-01,effective 9909151999-09-24024 September 1999 Informs That There No Longer Exists Need to Maintain Millstone Unit 2 SRO License for CA Hines,License SOP-10741-01,effective 990915 05000336/LER-1999-001, Forwards LER 99-001-00 Re Thermal Reactor Power Limit That Was Exceeded.Commitments Made by Util Encl1999-09-20020 September 1999 Forwards LER 99-001-00 Re Thermal Reactor Power Limit That Was Exceeded.Commitments Made by Util Encl B17867, Requests Relief from Requirements of 10CFR50.55a(g),IAW ASME Section XI for Millstone,Unit 3.Util Requests Relief from Performing Visual Exam of Reactor Pressure Supports to Extent Required by Code for Class 1 Supports1999-09-17017 September 1999 Requests Relief from Requirements of 10CFR50.55a(g),IAW ASME Section XI for Millstone,Unit 3.Util Requests Relief from Performing Visual Exam of Reactor Pressure Supports to Extent Required by Code for Class 1 Supports B17876, Informs That Util Will Adopt Last Approved Northeast Util QA Program (Nuqap) Tr,Rev 21,dtd 990630,as Unit 1 Nuqap,Per Decision to Permanently Cease Operations at Subject Plant1999-09-16016 September 1999 Informs That Util Will Adopt Last Approved Northeast Util QA Program (Nuqap) Tr,Rev 21,dtd 990630,as Unit 1 Nuqap,Per Decision to Permanently Cease Operations at Subject Plant B17865, Provides NRC Staff with Updated Proposed Rev of FSAR Section 14.6.3, Radiological Consequences of SG Tube Failure. Updated Proposed Rev Will Replace Info Provided in Attachment 3 of Initial Submittal1999-09-16016 September 1999 Provides NRC Staff with Updated Proposed Rev of FSAR Section 14.6.3, Radiological Consequences of SG Tube Failure. Updated Proposed Rev Will Replace Info Provided in Attachment 3 of Initial Submittal B17859, Forwards up-to-date Distribution Lists for NRC Correspondence to NNECO & NUSCO.Side-bars Indicate Changes from Previous Lists Provided to NRC on 9801281999-09-15015 September 1999 Forwards up-to-date Distribution Lists for NRC Correspondence to NNECO & NUSCO.Side-bars Indicate Changes from Previous Lists Provided to NRC on 980128 B17881, Forwards NRC Form 398 & NRC Form 396 for Le Olsen,License SOP-10398-2.Encl Withheld Per 10CFR2.790(a)(6)1999-09-15015 September 1999 Forwards NRC Form 398 & NRC Form 396 for Le Olsen,License SOP-10398-2.Encl Withheld Per 10CFR2.790(a)(6) B17880, Forwards NRC Form 398 & NRC Form 396 for Rf Martin,License SOP-10397-0.Encls Withheld Per 10CFR2.790(a)(6)1999-09-15015 September 1999 Forwards NRC Form 398 & NRC Form 396 for Rf Martin,License SOP-10397-0.Encls Withheld Per 10CFR2.790(a)(6) B17882, Forwards NRC Forms 398 & 369 in Support of License Renewal for Bb Parrish,License SOP-10399-2.Encl Withheld Per 10CFR2.790(a)(6)1999-09-15015 September 1999 Forwards NRC Forms 398 & 369 in Support of License Renewal for Bb Parrish,License SOP-10399-2.Encl Withheld Per 10CFR2.790(a)(6) B17872, Informs of Election to Consolidate Previous Commitments Re Work Observation Program with Two New Programmatic Commitments Listed in Attachment 11999-09-14014 September 1999 Informs of Election to Consolidate Previous Commitments Re Work Observation Program with Two New Programmatic Commitments Listed in Attachment 1 B17838, Forwards Revs 34 & 35 to Physical Security Plan.Explanation of Changes Provided as Attachment 1.Without Encls1999-09-10010 September 1999 Forwards Revs 34 & 35 to Physical Security Plan.Explanation of Changes Provided as Attachment 1.Without Encls ML20211J9291999-09-0303 September 1999 Forwards mark-ups & Retypes of Proposed Conforming License Changes Required in Connection with Transfers Being Sought in 990615 Application of Montaup Electric Co & New England Power Co for Transfer of Licenses & Ownership Interests ML20216H0591999-09-0202 September 1999 Responds to Re Issues Submitted by Cullen on Behalf of Several Petitioners Concerning Offsite Emergency Prepardeness for Millstone Nuclear Power Station 05000336/LER-1999-010, Forwards LER 99-010-00,documenting 990804 Event of Failure to Perform ASME Section XI IST on Pressurizer Relief Line Flow Control Sample Valve Following Maint Activities.List of Util Commitments Contained in Attachment 11999-09-0202 September 1999 Forwards LER 99-010-00,documenting 990804 Event of Failure to Perform ASME Section XI IST on Pressurizer Relief Line Flow Control Sample Valve Following Maint Activities.List of Util Commitments Contained in Attachment 1 CY-99-111, Submits Clarification of Changes Made to Connecticut Yankee QA Program,Per Util 990810 Submittal.Change Will Be Submitted to NRC in Dec 1999 as Part of Annual Update1999-09-0202 September 1999 Submits Clarification of Changes Made to Connecticut Yankee QA Program,Per Util 990810 Submittal.Change Will Be Submitted to NRC in Dec 1999 as Part of Annual Update ML20211N9241999-09-0101 September 1999 Forwards Document Classification Form for Insertion Into Emergency Planning Services Department Procedures B17851, Forwards Semiannual fitness-for-duty Program Performance Data for 990101-990630 for Millstone Nuclear Power Station, Units 1,2 & 3,IAW 10CFR26.71(d)1999-08-27027 August 1999 Forwards Semiannual fitness-for-duty Program Performance Data for 990101-990630 for Millstone Nuclear Power Station, Units 1,2 & 3,IAW 10CFR26.71(d) B17855, Forwards NRC Forms 398 & 396 in Support of License Renewal for SRO TE Grilley,SOP-4053-04.Encl Withheld,Per 10CFR2.7901999-08-17017 August 1999 Forwards NRC Forms 398 & 396 in Support of License Renewal for SRO TE Grilley,SOP-4053-04.Encl Withheld,Per 10CFR2.790 B17849, Forwards Second Quarter Backlog Performance Rept for 1999, Which Represents Fourth Rept on Mnps Performance Since Restart of Unit 3 & First Status Update for Unit 2.No Regulatory Commitments Are Contained in Ltr1999-08-16016 August 1999 Forwards Second Quarter Backlog Performance Rept for 1999, Which Represents Fourth Rept on Mnps Performance Since Restart of Unit 3 & First Status Update for Unit 2.No Regulatory Commitments Are Contained in Ltr B17854, Forwards Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 2,per TS 6.9.1.7.Revised Repts for May & June Also Encl Which Reflect Correct Faulty Printometer Readings1999-08-14014 August 1999 Forwards Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 2,per TS 6.9.1.7.Revised Repts for May & June Also Encl Which Reflect Correct Faulty Printometer Readings B17850, Forwards First Lhc Quarterly Assessment Rept for Assessment Performed 990621 to 990701.NNECO Taking Appropriate Actions to Address Observations in Rept1999-08-11011 August 1999 Forwards First Lhc Quarterly Assessment Rept for Assessment Performed 990621 to 990701.NNECO Taking Appropriate Actions to Address Observations in Rept B17837, Forwards COLR for Cycle 7, for Millstone Unit 3,IAW TS 6.9.1.6.Explanation of Changes to COLR Also Encl1999-08-0707 August 1999 Forwards COLR for Cycle 7, for Millstone Unit 3,IAW TS 6.9.1.6.Explanation of Changes to COLR Also Encl B17657, Requests Schedular Exemption from Emergency Plan Exercise Requirements of 10CFR50,App E,Part Iv,Section F,Paragraph 2.c.Requests That Nrc/Fema Evaluated Exercise Be Conducted in Mar 2000 Rather than Sept 19991999-08-0303 August 1999 Requests Schedular Exemption from Emergency Plan Exercise Requirements of 10CFR50,App E,Part Iv,Section F,Paragraph 2.c.Requests That Nrc/Fema Evaluated Exercise Be Conducted in Mar 2000 Rather than Sept 1999 B17845, Forwards Revised Commitment for Surveillance Scheduling & Tracking.Options for Surveillance Scheduling & Tracking Methodologies to Be Incorporated in Standardized Station Surveillance Program Are Currently Being Reconsidered1999-08-0202 August 1999 Forwards Revised Commitment for Surveillance Scheduling & Tracking.Options for Surveillance Scheduling & Tracking Methodologies to Be Incorporated in Standardized Station Surveillance Program Are Currently Being Reconsidered CY-99-048, Forwards Cyap Rept CY-HP-0031,Rev 0, Bounding Dose Assessment for Offsite Radioactive Matls1999-07-29029 July 1999 Forwards Cyap Rept CY-HP-0031,Rev 0, Bounding Dose Assessment for Offsite Radioactive Matls B17831, Informs NRC Staff That Change 3 to Rev 25 of Mnps Emergency Plan Was Implemented on 990715.Change Removes Facility Organizational Charts from Emergency Plan & Identifies Relocation to Nuqap1999-07-26026 July 1999 Informs NRC Staff That Change 3 to Rev 25 of Mnps Emergency Plan Was Implemented on 990715.Change Removes Facility Organizational Charts from Emergency Plan & Identifies Relocation to Nuqap B17834, Forwards Proprietary Revised NRC Form 398,which Certifies That SL Doboe Has Completed Eligibility Requirements for Sro,Per 10CFR55.31.Proprietary Info Withheld1999-07-20020 July 1999 Forwards Proprietary Revised NRC Form 398,which Certifies That SL Doboe Has Completed Eligibility Requirements for Sro,Per 10CFR55.31.Proprietary Info Withheld B17811, Submits Response to NRC AL 99-02,requesting That Licensees Provide Numerical Estimates of Licensing Actions to Be Expected to Be Submitted in Fy 2000 & 20011999-07-20020 July 1999 Submits Response to NRC AL 99-02,requesting That Licensees Provide Numerical Estimates of Licensing Actions to Be Expected to Be Submitted in Fy 2000 & 2001 B17836, Forwards Revised NRC Form 396 & Supporting Physician Rept for Licensed Operator Restricted from Licensed Duties, Effective 990628,due to Medical Condition.Without Encl1999-07-20020 July 1999 Forwards Revised NRC Form 396 & Supporting Physician Rept for Licensed Operator Restricted from Licensed Duties, Effective 990628,due to Medical Condition.Without Encl CY-99-066, Forwards Revised Plan for Recovery of Licensed Matl from Offsite Locations.Completion of Implementation of Plan During Summer of 1999 Is Planned,Contingent on Support Extended by Property Owners,Weather & Uncontrolled Factors1999-07-20020 July 1999 Forwards Revised Plan for Recovery of Licensed Matl from Offsite Locations.Completion of Implementation of Plan During Summer of 1999 Is Planned,Contingent on Support Extended by Property Owners,Weather & Uncontrolled Factors ML20210S9911999-07-18018 July 1999 Requests NRC Intervene for All Shareholders of New England Electric System & to Help with Merger with National Grid Group & That NRC Petition Security & Exchange Commission to Investigate Matter Relative to No Shareholder Options B17835, Forwards Rev 33 to Millstone Station Physical Security Plan, Per 10CFR50.54(p)(2).Licensee Determined That Changes Do Not Decrease Effectiveness of Plan.Rev Withheld from Public Disclosure,Per 10CFR2.790(d)(1)1999-07-16016 July 1999 Forwards Rev 33 to Millstone Station Physical Security Plan, Per 10CFR50.54(p)(2).Licensee Determined That Changes Do Not Decrease Effectiveness of Plan.Rev Withheld from Public Disclosure,Per 10CFR2.790(d)(1) B17818, Provides NRC Staff with Change to TS Bases Sections 3/4.5.2 & 3/4.5.3, ECCS Subsystems for Info Only.Change Was Reviewed & Approved by Unit 3 Plant Operations Review Committee IAW Provisions of 10CFR50.591999-07-16016 July 1999 Provides NRC Staff with Change to TS Bases Sections 3/4.5.2 & 3/4.5.3, ECCS Subsystems for Info Only.Change Was Reviewed & Approved by Unit 3 Plant Operations Review Committee IAW Provisions of 10CFR50.59 B17824, Forwards Monthly Oeprating Rept for June 1999 & Revised Monthly Operating Rept for May 1999 for Millstone Unit 21999-07-13013 July 1999 Forwards Monthly Oeprating Rept for June 1999 & Revised Monthly Operating Rept for May 1999 for Millstone Unit 2 ML20212K1701999-07-13013 July 1999 Submits Concerns Re Millstone & Continued Lack of Emergency Mgt Plan for Eastern Long Island.Nrc Should Provide Adequate Emergency Planning in Case of Radiological Accident B17816, Provides Certification That M Lettrich,Has Completed Eligibility Requirements,Per 10CFR55.31 for Operator License.Util Requests That Licensing Action Be Taken for Named Individual1999-07-0101 July 1999 Provides Certification That M Lettrich,Has Completed Eligibility Requirements,Per 10CFR55.31 for Operator License.Util Requests That Licensing Action Be Taken for Named Individual ML20209C3911999-06-30030 June 1999 Forwards TS Page 6-3 for Haddam Neck Plant 1999-09-03
[Table view] Category:UTILITY TO NRC
MONTHYEARA08900, Responds to Expressing NRC Views on Access to Util Internal or third-party Assessment Repts.Believes Internal Analysis to Support Amend of One of Util NRC OLs to Authorize Higher Power Level Is within NRC Purview & Access1990-09-11011 September 1990 Responds to Expressing NRC Views on Access to Util Internal or third-party Assessment Repts.Believes Internal Analysis to Support Amend of One of Util NRC OLs to Authorize Higher Power Level Is within NRC Purview & Access ML20064A8071990-09-11011 September 1990 Forwards Core Operating Limits Rept for Four & Three Loop Operation,Per Tech Spec 6.9.1.6.d B13628, Forwards Correction to Error Discovered in Util 900727 Response to Notice of Violation from Insp Rept 50-336/90-09. Statement Corrected to Read That Contract Personnel That Have long-term Assignments,Certified as Testing Personnel1990-09-0707 September 1990 Forwards Correction to Error Discovered in Util 900727 Response to Notice of Violation from Insp Rept 50-336/90-09. Statement Corrected to Read That Contract Personnel That Have long-term Assignments,Certified as Testing Personnel B13624, Forwards Addl Info Re Relief Request from ASME Code Section XI Requirements for Temporary Repair to Piping Adjacent to Valve 2-SW-97A,per 900817 Telcon1990-09-0505 September 1990 Forwards Addl Info Re Relief Request from ASME Code Section XI Requirements for Temporary Repair to Piping Adjacent to Valve 2-SW-97A,per 900817 Telcon A08977, Advises of Commitment to Install Hardened Wetwell Vent at Facility,In Response to NRC .Util Will Be Proceeding W/Initial Design & Engineering of Hardened Vent, to Support Installation During 1993 Refueling Outage1990-09-0404 September 1990 Advises of Commitment to Install Hardened Wetwell Vent at Facility,In Response to NRC .Util Will Be Proceeding W/Initial Design & Engineering of Hardened Vent, to Support Installation During 1993 Refueling Outage B13626, Informs That Info Provided in Re safety-related Equipment Classification Programs Also Applicable for Unit 3 of Facility1990-08-31031 August 1990 Informs That Info Provided in Re safety-related Equipment Classification Programs Also Applicable for Unit 3 of Facility B13596, Forwards Millstone Unit 3 Individual Plant Exam for Severe Accident Vulnerabilities, Per Generic Ltr 88-20.Rept Identified That No Major Severe Accident Vulnerabilities Requiring Corrective Action Needed1990-08-31031 August 1990 Forwards Millstone Unit 3 Individual Plant Exam for Severe Accident Vulnerabilities, Per Generic Ltr 88-20.Rept Identified That No Major Severe Accident Vulnerabilities Requiring Corrective Action Needed B13622, Forwards Crdr Human Engineering Discrepancy Info for Plant1990-08-30030 August 1990 Forwards Crdr Human Engineering Discrepancy Info for Plant B13618, Forwards Addl Info on Util 900815 Relief Request from ASME Code Section XI Requirements,Per 10CFR50.55a(g)(6)(i),for Repairs to Pipe 3SWP-006-050-031990-08-24024 August 1990 Forwards Addl Info on Util 900815 Relief Request from ASME Code Section XI Requirements,Per 10CFR50.55a(g)(6)(i),for Repairs to Pipe 3SWP-006-050-03 ML20059C2061990-08-23023 August 1990 Forwards Vols 1 & 2 to Semiannual Radioactive Effluents Release Rept Jan-June 1990, Per 10CFR50.36a.Rept Includes Summary of Quantities of Solid Radwaste & Liquid & Gaseous Effluents A08918, Responds to Notice of Violation & Proposed Imposition of Civil Penalty Re Insp Rept 50-245/90-08.Mitigation of Civil Penalty Requested.Corrective Action:List of Procedural Changes Provided1990-08-22022 August 1990 Responds to Notice of Violation & Proposed Imposition of Civil Penalty Re Insp Rept 50-245/90-08.Mitigation of Civil Penalty Requested.Corrective Action:List of Procedural Changes Provided B13617, Requests NRC Revise Confirmatory Order for Plant to Specify New Completion Date of Cycle 16 Refueling Outage for Item II.E.1.2.Util Intends to Implement Design Change During Next Refueling Outage to Resolve Listed Issues1990-08-22022 August 1990 Requests NRC Revise Confirmatory Order for Plant to Specify New Completion Date of Cycle 16 Refueling Outage for Item II.E.1.2.Util Intends to Implement Design Change During Next Refueling Outage to Resolve Listed Issues B13615, Requests That 900705 Request for Amend to License DPR-61 Be Approved on Emergency Basis & That Temporary Waiver of Compliance from Tech Spec 4.4.6.2.1.g Be Given Until NRC Acts on Emergency Amend1990-08-20020 August 1990 Requests That 900705 Request for Amend to License DPR-61 Be Approved on Emergency Basis & That Temporary Waiver of Compliance from Tech Spec 4.4.6.2.1.g Be Given Until NRC Acts on Emergency Amend B13611, Forwards, Semiannual Radioactive Effluents Release Rept for Jan-June 19901990-08-16016 August 1990 Forwards, Semiannual Radioactive Effluents Release Rept for Jan-June 1990 B13610, Requests Relief from ASME Boiler & Pressure Vessel Code Section XI Requirements Re Mods to Pipe 3SWP-006-050-03. Results of Insps & Required Repairs Will Determine Schedule for Future Insps1990-08-15015 August 1990 Requests Relief from ASME Boiler & Pressure Vessel Code Section XI Requirements Re Mods to Pipe 3SWP-006-050-03. Results of Insps & Required Repairs Will Determine Schedule for Future Insps B13595, Notifies NRC That Utils Volunteer to Participate in Emergency Response Data Sys Project for All Four Nuclear Units,Per Generic Ltr 89-15 & NUREG-13941990-08-14014 August 1990 Notifies NRC That Utils Volunteer to Participate in Emergency Response Data Sys Project for All Four Nuclear Units,Per Generic Ltr 89-15 & NUREG-1394 B13602, Submits Addendum to Plant Control Room Design Review Summary Rept,Per .Lists 10CFR50 App R-related Mods Outside Control Room That Could Not Be Reviewed Until After Final Implementation of Changes1990-08-14014 August 1990 Submits Addendum to Plant Control Room Design Review Summary Rept,Per .Lists 10CFR50 App R-related Mods Outside Control Room That Could Not Be Reviewed Until After Final Implementation of Changes B13607, Requests Relief from ASME Code Section XI to Reflect Mod to Piping Adjacent to Valve 2-SW-97A,in Response to Generic Ltr 90-051990-08-10010 August 1990 Requests Relief from ASME Code Section XI to Reflect Mod to Piping Adjacent to Valve 2-SW-97A,in Response to Generic Ltr 90-05 B13580, Discusses Revised Tech Spec Conversion Program,Reflecting Conversion of Tech Spec to Westinghouse Sts.Future Upgrade of Tech Specs Should Be Conducted on Voluntary Basis Consistent W/Nrc Policy Statement1990-08-10010 August 1990 Discusses Revised Tech Spec Conversion Program,Reflecting Conversion of Tech Spec to Westinghouse Sts.Future Upgrade of Tech Specs Should Be Conducted on Voluntary Basis Consistent W/Nrc Policy Statement A08845, Responds to NRC Backfit Analyses of Hardened Wetwell Vent, Contained in .Benefit of Installing Hardened Wetwell Vent to Satisfy Basic Design Objective of Preventing core-melt Event Not Sufficient for Immediate Decision1990-08-0808 August 1990 Responds to NRC Backfit Analyses of Hardened Wetwell Vent, Contained in .Benefit of Installing Hardened Wetwell Vent to Satisfy Basic Design Objective of Preventing core-melt Event Not Sufficient for Immediate Decision ML20058M8321990-08-0707 August 1990 Discusses Spent Fuel Racks Poison Surveillance Coupon Boraflex Degradation.Visual Exam of Remaining Surveillance Coupons Revealed Similar Situation Existed in All Coupon Samples ML20058N2181990-08-0707 August 1990 Notification of Change in Senior Operator Status.Util Determined That Need to Maintain Senior OL of LS Allen No Longer Exists.Determination Effective 900719 B13603, Withdraws 900731 Request for Temporary Waiver of Compliance W/Tech Spec 3.7.1.2 Re Inoperability of Auxiliary Feedwater Pumps1990-08-0202 August 1990 Withdraws 900731 Request for Temporary Waiver of Compliance W/Tech Spec 3.7.1.2 Re Inoperability of Auxiliary Feedwater Pumps B13590, Responds to NRC 900718 Request for Addl Info Re Util 900418 Request for Schedular Exemption from 10CFR50,App E,Section IV.F.3 to Allow Dec 1990 Full Participation Exercise to Be Exchanged W/Oct 1991 Partial Participation Exercise1990-08-0101 August 1990 Responds to NRC 900718 Request for Addl Info Re Util 900418 Request for Schedular Exemption from 10CFR50,App E,Section IV.F.3 to Allow Dec 1990 Full Participation Exercise to Be Exchanged W/Oct 1991 Partial Participation Exercise B13601, Requests Temporary Waiver of Compliance from Tech Spec 3.7.1.2,allowing Plant to Remain in Mode 3 for Addl 14 Days Beyond Current Action Statement Limits W/One or of Two Auxiliary Feedwater Pumps Inoperable1990-07-31031 July 1990 Requests Temporary Waiver of Compliance from Tech Spec 3.7.1.2,allowing Plant to Remain in Mode 3 for Addl 14 Days Beyond Current Action Statement Limits W/One or of Two Auxiliary Feedwater Pumps Inoperable A08881, Responds to NRC Re Violations Noted in Insp Rept 50-423/90-08.Corrective Action:Operators Directly Involved W/Event Removed from Licensed Duties & Counseled by Operations Manager on Causes of Event1990-07-31031 July 1990 Responds to NRC Re Violations Noted in Insp Rept 50-423/90-08.Corrective Action:Operators Directly Involved W/Event Removed from Licensed Duties & Counseled by Operations Manager on Causes of Event B13594, Forwards Rev 13 to Physical Security Plan.Rev Withheld (Ref 10CFR73.21(b) & 2.790(a))1990-07-30030 July 1990 Forwards Rev 13 to Physical Security Plan.Rev Withheld (Ref 10CFR73.21(b) & 2.790(a)) ML20055J4621990-07-27027 July 1990 Advises That Need to Maintain OL or Senior OL for Listed Individuals No Longer Exists,Effective 900701 B13585, Provides Supplemental Response to Generic Ltr 89-19 Re Request for Action Concerning Resolution of Unresolved Safety Issue A-47.Plant Procedures Modified to Provide Operability Verification of Steam Generator Protection Sys1990-07-26026 July 1990 Provides Supplemental Response to Generic Ltr 89-19 Re Request for Action Concerning Resolution of Unresolved Safety Issue A-47.Plant Procedures Modified to Provide Operability Verification of Steam Generator Protection Sys A08565, Responds to NRC 900302 Request for Addl Info Re LPCI Swing Bus Transfer Design & Single Failure Vulnerabilities1990-07-26026 July 1990 Responds to NRC 900302 Request for Addl Info Re LPCI Swing Bus Transfer Design & Single Failure Vulnerabilities B13592, Requests Extension to Respond to NRC Backfit Analyses of Hardened Wetwell Vent1990-07-24024 July 1990 Requests Extension to Respond to NRC Backfit Analyses of Hardened Wetwell Vent ML20063P9791990-07-23023 July 1990 Notification of Change in SL Jackson Status Effective 900701,due to Permanent Reassignment within Util B13566, Advises That Util Has Reasonable Assurance That Safety Relief Valves Operable & Will Perform as Expected Until Next Outage1990-07-20020 July 1990 Advises That Util Has Reasonable Assurance That Safety Relief Valves Operable & Will Perform as Expected Until Next Outage B13563, Discusses Util Comprehensive Review of Options Re Degraded Grid Undervoltage Protection.Confirms Previous Conclusion That Splitting Loss of Normal Power Logic Would Have Overall Adverse Impact on Plant Safety1990-07-20020 July 1990 Discusses Util Comprehensive Review of Options Re Degraded Grid Undervoltage Protection.Confirms Previous Conclusion That Splitting Loss of Normal Power Logic Would Have Overall Adverse Impact on Plant Safety B13571, Clarifies 900625 Tech Spec Change Request Re Limit of 160 Failed Fuel Rods for Cycle 16 Operation1990-07-19019 July 1990 Clarifies 900625 Tech Spec Change Request Re Limit of 160 Failed Fuel Rods for Cycle 16 Operation ML20055G5331990-07-18018 July 1990 Forwards Decommissioning Financial Assurance Certification Rept B13588, Corrects 900703 Submittal of Results of Second in-cycle Insp of Steam Generators.All Tubes W/Cracks Stacked & Plugged1990-07-18018 July 1990 Corrects 900703 Submittal of Results of Second in-cycle Insp of Steam Generators.All Tubes W/Cracks Stacked & Plugged A08822, Submits Addl Info Requested Re Util Response to Generic Ltr 88-11, Radiation Embrittlement of Reactor Vessel Matls. Charpy Impact Use Values for Welds Provided in Evaluation of Irradiated Capsule W-971990-07-18018 July 1990 Submits Addl Info Requested Re Util Response to Generic Ltr 88-11, Radiation Embrittlement of Reactor Vessel Matls. Charpy Impact Use Values for Welds Provided in Evaluation of Irradiated Capsule W-97 B13569, Forwards, Haddam Neck Plant Decommissioning Financial Assurance Certification Rept1990-07-18018 July 1990 Forwards, Haddam Neck Plant Decommissioning Financial Assurance Certification Rept B13587, Requests Temporary Waiver of Compliance from Tech Spec 3.5.F.2 Re Emergency Diesel Generator (EDG) Limiting Condition for Operation.Waiver Would Extend Available Time to Repair Damaged Electrical Components1990-07-16016 July 1990 Requests Temporary Waiver of Compliance from Tech Spec 3.5.F.2 Re Emergency Diesel Generator (EDG) Limiting Condition for Operation.Waiver Would Extend Available Time to Repair Damaged Electrical Components ML20055E6791990-07-0606 July 1990 Responds to NRC Bulletin 88-008, Thermal Stresses in Piping Connected to Rcs. All Socket Welded Joints from Header Isolation motor-operated Valves to RCS for All 4 Loops Examined.No Recordable Indications Found ML20055D3461990-07-0303 July 1990 Responds to NRC Bulletin 90-001 Re Loss of Fill Oil Transmitters Mfg by Rosemount.Operability Determinations Performed & Documented for All Rosemount 1153 & 1154 Transmitters at Facility ML20055D3481990-06-29029 June 1990 Forwards Addl Info Re Facility Crdr & Isap,Including Justification for Human Engineering Discrepancies Dispositioned for No Corrective Action ML20055D7191990-06-29029 June 1990 Amends 900604 Rev 13 to QA Program B13545, Forwards Rev 3 to Updated FSAR for Millstone Unit 31990-06-29029 June 1990 Forwards Rev 3 to Updated FSAR for Millstone Unit 3 B13531, Forwards Rev 8 to Updated FSAR for Millstone Unit 21990-06-29029 June 1990 Forwards Rev 8 to Updated FSAR for Millstone Unit 2 B13564, Provides NRC W/Info Re Plant Pressurizer as follow-up to 900607 Meeting.Info Particularly Concerns Disposition of Three Indications on Pressurizer Inner Surface & Discussion of Resolution of Previous Indication1990-06-29029 June 1990 Provides NRC W/Info Re Plant Pressurizer as follow-up to 900607 Meeting.Info Particularly Concerns Disposition of Three Indications on Pressurizer Inner Surface & Discussion of Resolution of Previous Indication B13550, Responds to Generic Ltr 90-04, Request for Info on Status of Generic Safety Issues Resolved W/Imposition of Requirements or Corrective Actions. Implementation & Completion Tables for staff-imposed Requirements Encl1990-06-27027 June 1990 Responds to Generic Ltr 90-04, Request for Info on Status of Generic Safety Issues Resolved W/Imposition of Requirements or Corrective Actions. Implementation & Completion Tables for staff-imposed Requirements Encl B13499, Forwards Corrected Tech Specs Page 3/4 9-1 for Incorporation Into Proposed Amend 36 to License DPR-21 Re Auxiliary Electrical Sys1990-06-26026 June 1990 Forwards Corrected Tech Specs Page 3/4 9-1 for Incorporation Into Proposed Amend 36 to License DPR-21 Re Auxiliary Electrical Sys ML20043F8721990-06-11011 June 1990 Corrects Name of Vendor Supplying Replacement Plug Valves, Per Util 900511 Ltr.Replacement Bolts,Not Valves,Purchased from Cardinal Industrial Products Corp 1990-09-07
[Table view] |
Text
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General Offices
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5 March 22,1985
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Docket Nos. 50-213 g 50-245 a 50-336 _
B11411 -
7 Mr. R. W. Starostecki, Director i SALP Board Chairman 4 Division of Project and Resident Programs d U. S. Nuclear Regulatory Commission -i 631 Park Avenue y King of Prussia, PA 19406 a 2
Mr. Lester Rubenstein, Assistant Director j Core and Plant Systems a Office of Nuclear Reactor Regulation j U. S. Nuclear Regulatory Commission j Washington, D. C. 20555 4 5
Mr. Warren Minners, Chief g Safety Program Evaluation Branch j Office of Nuclear Reactor Regulation 4 U. S. Nuclear Regulatory Commission :
Washington, D. C. 20555 =
E Gentlemen:
Haddam Neck Plant, Millstone Nuclear Power Station Unit Nos. I and 2 d Systematic Appraisal of Licensee Performance 4 a
As you are no doubt aware from previous meetings with us regarding the SALP ]
program, Northeast Utilities (NU) places high priority on achieving excellence in -
our endeavors. Category I ratings in all areas of activity evaluated by that =
program would represent one signal that this goal is being realized. Our commitment to strive for Category I ratings originates from NU executive management and is one element of our primary corporate objective of striving -
for excellence in the maintenance of nuclear safety. Given the scope and depth -
of SALP reviews, achievement of superior ratings provides an indication that our management controls are functioning properly. Ratings lower than Category I -
identify potential areas for improvement, j In the past, SALP meetings have occurred subsequent to publicacion of the initial i NRC SALP report. As a result, we believe that the initial reports have at times j failed to take into account pertinent information and otherwise could have been i strengthened by an exchange between ourselves and the NRC. To minimize the -,
chances of this situation recurring, we are taking this opportunity prior to the -!
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convening of your;SALP Board for our three operating nuclear units to offer-isome of our perspectives on our level of performance during the past months.
~We believe that doing so may prove useful in your _ deliberations. We are
' addressing this document-to you in your respective capacities as lead SALP
_ participants (SALP Board . Chairman, or NRR Senior Executives) for our facilities. .
. Generally, we 'believe ' that the .nine. functional areas in which the NRC has :
chosen to evaluate license performance will provide an overall perspective of our operations. However, an evaluation of these areas exclusively does not, in our opinion, comprise the universe of those factors which should be considered in .
assessing ." licensee performance." Perhaps the most significant factor which we believe should be considered and which is not reflected in the nine functional areas is the extent to which a licensee attempts to further the depth and quality
- of the exchange with the regulators, both _in terms of interacting with the NRC ,
and participating actively in _ efforts . to disseminate needed information to 4
industry. NU has consistently adhered to the view that we are obliged to voice-our disagreement with NRC on any. issue involving public health and safety when _
we believe such disagreement is justified. We do so_ in the interest.of further Improving .the' regulatory process and assuring that through discussion and debate, all aspects of a proposed action are understood and considered by both
- NRC and NU.~ We sense that on occasion this corporate philosophy may have disturbed certain: NRC reviewers. However, we do' not believe that this E
(. philosophy should be counted against us in your SALP evaluation. - On the contrary, we believe~ it necessary and appropriate for us to vigorously interact with the Staff as necessary to ensure that public health and safety is maintained, particularly given the finite resources at the disposal of both NU and the NRC.
~'
Examples of = some. of our attempts to further improve the. quality of the regulatory process are enumerated in Attachment (1) to this letter. Many of them have their focus on providing the regulators with an opportunity to become
.more familiar with our plants, procedures and personnel. They are far ranging in scope, involving executive management down through the working level. Our former Chief Executive Officer (CEO) is the current chairman of the board of the Institute of Nuclear Power Operations (INPO). Northeast Utilities executive management is extremely active in numerous industry initiatives, having made several presentations' at public meetings.before the Commission 'as well as meeting with individual Commissioners where appropriate. NU management ,
personnel are extremely ' active in, and in many instances chair, various industry .
groups which are addressing a broad range of nuclear issues.
Regarding . day-to-day activities, our licensing staff attempts to be very -
- responsive to the NRC licensing project managers (LPMs). We attempt to respond to verbal inquiries quickly and accurately, arrange for all necessary meetings and/or conference calls, help the LPMs locate previously docketed
- 7 material, and provide express. mail service for both incoming and outgoing correspondence as circumstances require to ensure that priority issues are given
- priority treatment.. We believe that the recent briefings conducted by the new NRR Division of Licensing Director support the above perspective.
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o Another element of our corporate efforts to achieve excellence which may not
=be reflected in the nine functional categories NRC evaluates as part of SALP is the, extent to,which actions are implemented following a SALP evaluation in order to improve a licensee's level _of performance. Examples of these activities which have occurred since the most recent SALP report for our operating nuclear facilities are provided in Attachment (2) to this submittal. - Again, it is not all inclusive, but is illustrative of our commitment to strive for excellence.
- We note that this letter focuses; exclusively on those activities which we believe are relevant to the SALP process and which, based upon our knowledge of the process,' may not otherwise be fully ' considered. The fact that many other pertinent issues and documents are not discussed herein is not to suggest they are less important.
- We are aware that the 'NRC has developed procedures for the conduct of the
.SALP process and has acquired considerable experience over the .last several yea'rs in performing.SALP_ evaluations. In the spirit of further improving the
-process, we urge you to consider _ the areas of activity discussed above, as supplemented by the Attachments to this document. Further, we invite you to ask any questions which may arise during the conduct of the SALP evaluation for our facilities in the interest of eliminating points of confusion and enhancing the overall quality and' depth of the SALP evaluation process.
Feel free to contact us if any questions arise on this matter.
Very truly yours,
. CONNECTICUT YANKEE ATOMIC POWER COMPANY NORTHEAST. NUCLEAR ENERGY COMPANY
. W. G. Counsil Senior Vice President cc: T. E. Murley W. 3. Dircks V.' Stello, Jr.
H. R. Denton D. G. Eisenhut H. L. Thompson, 3r.
D. M. Crutchfield :
G. C. Lainas
- 3. A. Zwolinski
- 3. R. Miller i
. . g- _ .. ,
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.- Docket Nos. 50-213 ~
50-245 50-336
' Attachment 1 Haddam' Neck Plant Millstone Nuclear Power Station, Unit Nos. I and 2 Inputs to SALP Evaluation Process
-u j ,:
L, March,1985
- o. ..
The following items provide a summary description of various meetings, letters, or other transactions which we believe are relevant to the conduct of the SALP
' process for our facilities. In the interest of brevity, only a summary of each of -
the pertinent _ elements is provided below. Further elaboration can be provided if
.' desired by the NRC.
o Early in 1984, the NRC published its Policy and Planning Guidance as
' NUREG-0885. By letter dated February 2,_1984, we provided unsolicited -
- comments on this document. This submittal subsequently lead to a number of . meetings with the. EDO's . Staff regarding possible improvements in subsequent direction to the NRC Staff.
o- On - March 23, 1984, we provided a letter to V. Stello Jr. regarding the proposed _ Senior Manager Rule. We understand that senior staff management believed that this document . presented a worthwhile -
perspective different from that proposed by the Senior Manager Rule and as such, was forwarded to the Commission for their consideration. In November of 1984, the Commission disapproved the proposed rule.
o- 'In recognition of the importance to safety of reducing unscheduled plant trips, we have adopted corporate goals and initiatives to reduce unplanned
- trips and their subsequent challenges to safety systems. This program was discussed in summary fashion during a meeting with the CRGR in July of 1984.
o The issue of environmental qualification is one for which it has proven.to
~ be difficult to achieve closure. Given the long standing nature of the' issue and the turnover of both NRC staff and contractor personnel, we have periodically.provided to the staff a chronological listing of all documents
- exchanged between us and the NRC for each of our nuclear units. We have done ~so in the interest of facilitating the process by which the Staff can trace the basis-for closure of any individual aspect of the environmental qualification issue, o At the request of a senior staff manager, a letter was sent to H. R. Denton on July 15, 1984 regarding the involvement of the Nuclear Utility Task Action Committee.(NUTAC) and its attempts to achieve resolution of the 'l SPDS issue. !
~
l
'o : At the request of H. R. Denton, we entertained a visit in June of 1984 by <
the Environmental Programs Branch of the NRC to allow them to obtain additionalinformation regarding the quality of their work.
o During the 1984 refueling outage at Millstone Unit No.1, we entertained a visit by NRC contractors from EG&G to allow them to collect information on the decontamination process utilized as part of remedial action associated with the IGSCC issue.
o In August of 1984, representatives from Brookhaven National Labs, under contract with NRC, visited us to obtain information on implementation of our ALAR A programs, o In October of 1983, we entertained personnel from the NRC and Battelle
. Pacific Northwest Laboratories regarding their interest in biofouling in raw water systems.
I
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of The issue of the flooding at :the Haddam Neck Plant as' a result _of a
.Quabbin Reservoir dam failure consumed considerable resources within NU.
Numerous meetings were held involving the State of Connecticut, FEMA,-
NationalT Weather '= Service, and other organizations. NU personnel coordinated several visits on the part of the Staff to ensure that all of
-their questions were answered satisfactorily.
o- Severalidays 'before the' completion' of the 1984 refueling outage for .
- Millstone Unit No. J1, the staff telephoned us to request that we immediately provide a report of our IGSCC program and results of all inspections. Their original intention was to write an SER prior to startup.
While we. did not accept 'the~ verbal staff position that an SER was
' necessary prior. to_ startup, all requested information was gathered and submitted promptly by letter dated June 15,1984.
o As part of the resolution of the hydrogen recombiner issue for inerted r
BWR's, the NRC issued Generic Letter 84-09. As a result of questions and '
inquiries from the BWR community regarding the applicability of previous
- Northeast Utilities work on this issue, we hosted a seminar in our corporate offices on June 15,'1984 to review our analyses and answer questions. This was done in the interest of furthering industry-wide resolution of this issue.
- o. On July 17 and 18 'of 1984, we entertained a visit of the majority of the members of the Committee to Review Generic Requirements (CRGR).-
This visit involved discussions with numerous licensed personnel as well as
' discussions with numerous levels of NU management. Significant resources were expended in the interest of further improving communications and-obtaining a better appreciation of our respective viewpoints.
E o - Generic Letter 84-15 requested a considerable amount of information -
regarding diesel generator performance in the interest of resolving generic issue B-56. In- addition to this 'information, we ' included voluntarily information regarding the performance of the gas turbine at Millstone Unit
, No.1.
o, On July 31,'1984, W. G. Counsil was one of several industry spokesmen who provided information to the commission.on the important-to-safety issue.
- _
- At this meeting, Mr. Counsil represented the Utility Safety Classification .
, Group. This presentation ultimately led to a visit by four members of the,
, NRC~the following week at our Millstone facility to gather information on
- , the' treatment of equipment and components not classified as safety _
related. It is our~ understanding that this information was utilized in the development of the subsequent draft generic letter regarding the ATWS -
rule.
o In August of 1984, we entertained a visit on the part of several members of the NRC on the maintenance issue. This visit also consumed significant NU resources and was done in the interest of improving the then draft Staff Maintenance Program Plan.
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lo In' September of 1984, Harold Denton and several other staff members of NRR visited the Haddam Neck site as part of the resolution of a Differing Professional Opinion on the fire protection issue.
o~ In light of the safety significance of the reactor cavity pool seal issue at the Haddam' Neck Plant, NU initiated, and remains in the process of implementing, broad corrective actions. While many of these actions'are-
" utility specific, we have attempted to share our view of the safety
- significance of-this issue throughout the industry. In October of 1984 we
, hosted a seminar in.our corporate offices in an attempt to explain the
' details of the event,-its safety significance, and answer any questions.
Because of .short notice for. this meeting, a subsequent seminar was cohosted by Northeast Utilities and INPO on December 13, 1984. We believe this meeting was helpful in heightening industry awareness of the significance of this issue.
Regarding the Order Modifying License which was issued as a result of this tissue in December of 1984, our response was submitted to the NRC some two months . earlier than required. This action reflects our resolve' to address any potential safety issues swiftly and effectively.
o One of _the elements of our corporate strategy regarding steam generators at Millstone Unit No. 2 concerns a chemical cleaning process planned to occur during the 1985 refueling outage. While this process is governed by
~
the provisions _of 10 CFR 50.59 and as such no prior staff involvement is required, we voluntarily briefed the staff on December 5, 1984 in considerable detail regarding our planned process and its qualification. No' unanswered questions remained at the conclusion of this meeting.
o- - At_ the request of the Staff in December of 1984, we agreed to have the Staff conduct a review of our plant specific emergency operating -
procedures as well as the procedures generation package from which the -
plant specific procedures are prepared. It is our unde.rstanding that this differs from the normal. process when only the procedures generation -
package is reviewed by the Staff.
o As a representative from NUMARC, executive NU management worked with Senior Staff management and the Commission in the last quarter of 1984 and the first quarter of 1985 on the engineering expertise on shift
' issue. Extensive efforts were devoted towards development of a mutually agreeable and workable policy statement.
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o ' As part of an AIF. coordinated effort, NU executive management and other
. industry- executives' met .with several . Commissioners. Individually. in
- January,1985 to discuss approaches.to resolve several issues of importance to both the Commission and the industry. .
to . . ' In September of i 1984, - two . NU representatives participated in a Commission briefing,on the decommissioning issue. This briefing was intended to facilitate Commission' deliberations on a proposed rule on the subject, and familiarize them with the status of utility programs and State PUC activities dealing with decommissioning.
o On - 3anuary 3, '1985, we were notified of an NRC. endorsed activity regarding the National Science Foundation PRA Peer Review Panel. Some
-.two weeks later, NU hosted the first two day meeting of this Panel. The
. meeting included tours of the Millstone Station and familiarization with 1PRA' applications at NU.
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- p, Docket Nos. 50-213 30-245 50-336
. Attachment 2
. Haddam Neck Plant Millstone Nuclear Power Station, Unit Nos. I and 2 Follow-up to Previous SALP Report Actions March,1985
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Connecticut Yankee The NRC Systematic Assessment of Licensee Performance (SALP) report issued in October of 1983 gave the Haddam Neck Plant Category 1 ratings in all areas but.one. This one area was surveillance, in which Lthe Staff assigned a Category 2 rating. The Haddam Neck Plant's surveillance plan was broken into component parts and each component individually analyzed. These components and the plant's corrective actions are enumerated below. These component parts
< cover all deficiencies identified in'Part 4.4 of the SALP report for the Haddam Neck Plant..-
-COMPONENT: COMMENTS / ACTIONS
- 1) ' Data Base All Connecticut -Yankee (CY) department heads have updated their portion of -the data base for compliance .to. Technical Specifications. Additionally,' the Quality.-
Assurance _ Department, as required by procedure, has performed a complete data base- review. The data base will be maintained on the computer program.
- 2) Timing Systems Computerized systems have been expanded to include refueling, cold shutdown and all surveillances with frequencies less than a week. However, timing systems will only schedule any surveillance with - frequency greater than a week. The computerized system is the official CY Date Base.
- 3) Performance Since most surveillance fallings are improper performance, further . procedural guidance and training were needed.
CYSP-71 has been eliminated, and procedure L QA 1.2-11.1 enhanced to pick up any items implemented by CYSP-71 but not covered in QA 1.2-11.1.
Guidance on actions to take with incorrect procedures, procedure . corrections and compliance with procedures has been added ,
' to ACPs.
Using ACPs as source documents, CYAPCO has prepared departmental level instructions and provided training on the proper use of procedures.
4)' . Evaluations and Results Format for surveillance procedure sign-offs is:
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2i Performed by (Level I)
Approved by (Level II or greater)
Reviewed by, - (Level II or greater)
The " Approved by" must be Level II qualified
- as this is the point at which the surveillance
' is~ considered complete. The_ " Reviewed by"
.*. requires. a Level II : or greater, .. but : will s
t normally be a Level III.
The method of recording acceptance criteria on _' procedures has been - upgraded . for consistency and clarity and added to ACPs.
, . QA' - 1.2-11.2 has .been revised to include definitions of approved by and reviewed by.
Definition. of " performed by" was not
, required, being obvious.
- 5) Corrective Action QA 1.2-11.2 has been revised to provide
, guidance on acceptance criteria and need for Plant Incident Report (PIR) initiation.
- 6) Compliance Verification .Each department _ - head responsible .for surveillances has provided - their superintendent a program for ' continuing surveillance compliance verification. Quality.
Assurance audits, NRC audits, etc., are not used as the key evaluation factors for compliance -- verification,- unless major problems are found. _ Additionally, the I&C Surveillance Feedback Sheet which requests feedback _ from personnel performing' surveillances when a surveillance is Improper,-
incorrect or is difficult to use has been reviewed by each , department for' implementation as part of their departmental programs.
- 7) Records The computerized schedule has been evaluated as a "living schedule" to replace the forwarding schedule.
Review .and approval of surveillance procedures prior to a start-up is a departmental responsibility and is monitored,
- , but results indicate no action is needed at this time. ;
'8) Miscellaneous (1) A surveillance as defined in 10 CFR
[
50.36(c)(3) will mean only technical L specification commitments. Other items l .
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can be on the computerized schedule and proceduralized but will not be a surveillance test. - Procedures will be r.
reformatted . to meet . this . definition during the ' normal biennial procedure review process. Scheduled completion of
, all procedures is July 31,1986.
(2) A standard method . for acceptance criteria format has been developed.
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Millstone Unit No.1 The NRC Systematic Evaluation of Licensee Performance (SALP) report issued in October of 1983 gave Millstone Unit No._1 Category I ratings in all areas but
- three. - The areas which received a Category 2 rating, the NRC concerns in these
- areas and NNECO corrective actions are listed below:
- 1) ~ Plant Operations
- Concern:-
On. July. 20-21, 1983 a radioactive . liquid discharge was unintentionally made for 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> due to failure to secure flush water through an effluent radiation monitor.
Corrective Action:
All operations personnel, in addition to those directly involved with the incident, have been reminded of their responsibilities and the importance
-of following station procedures. Procedure changes have been made to eliminate ^ unnecessary flushes by specifying the condition for which flushing is required. Procedure changes have also been made to include dual valve verification for terminating the flush of the sample chamber.
Concern:
An incident in March 1983 involved incorrect valve line-ups for sensors in the Reactor Protection System. This problem was previously identified in 1981.
Corrective Action:
Methods were implemented to control safety-related instrument valves to prevent recurrence of incidents of this nature. Personnel involved with the calibration and adjustment of safety-related instruments have been
- reminded of. the importance of proper restoration . methods , when performing surveillance and maintenance. Surveillance data sheets were revised to include all valve numbers and dual check-off/ initial spaces for every valve manipulated during surveillance and calibration.
Concern:
i
!' The Emergency Gas Turbine Generator has been allowed to deteriorate to a point that, during the appraisal period, problems have occurred with the gas turbine and its controls and the generator voltage regulator.
Corrective Action:
Instrument folders have been established for the governor control units as well as the drytest/ analog troubleshooting instrumentation. Key personnel monitor each gas turbine surveillance start and record selected gas turbine parameters. Maintenance was performed on the voltage
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L 1 regulator' during the recent refueling outage to replace defective parts and clean oxidation from contact surfaces. Installation of a dehumidifier for the voltage regulator cabinet precludes moisture intrusion.
- 2) : Surveillance Concern:
Surveillance ~ procedures had not been revised to include an independent
- verification of system restoration.
Corrective Action:
Surveillance procedures were . reviewed and modified as necessary to include an independent check for. system restoration. Also, surveillance data sheets were revised to include all valve numbers and dual check ~
off/ initial spaces for every valve manipulated during surveillances and calibration.
- 3) - Emergency Preparedness Concern:
Installation of the High-RangelMonitoring and Sampling Systems for the Unit I stack and the Unit 2 vent was not completed.
Corrective Action:
- Both monitors have been redesigned to allow prener calibration, and are -
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operational and in service at this time.
Concern:
Lesson' plans for training of each functional area of the emergency response organization were lacking.
Corrective Action: -
The Training Department individual dedicated to emergency plan training has developed lesson plans and is currently conducting training sessions.
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Millstone Unit No. 2 4 ,
^
The NRC Systematic' Evaluation of Licensee Performance (SALP) report issued-
=in October of 1983 gave Millstone Unit No. 2 Category I ratings in all areas but three. These three areas received a Category 2 rating. NRC concerna in these -
' areas and corrective actions taken by NNECO are listed below. -
iPlant Operations
- 1)' ~ Concern:
~
LAn aggressive program 1for improvement was not' evident in the on-site -
safety committee's . performance. The licensee, through :the safety cornmittee does .not effectively task all ' personnel,. organizations and -
contractors.
- _ Corrective Action:
The PORC review process was studied and changes implementsd. Major changes were an expansion of the PDCR review process, prior review of major procedure revisions and new procedures, better definition of the use
- of ,' subcommittees,' and' responsibilities . review during annual _PORC training. ' Particulars of the expansion of the PDCR process are a more detailed line revie~w of the PDCR before being submitted to PORC,' prior to review by 'PORC members and more detailed. presentations for the complex changes. In addition to the . review' of the PORC process, corporate-wide changes have been instituted to more clearly define safety .
. evaluation requirements and these improvements are being monitored by.
- P O R C .;
- 32) Concern:
-In two instances important equipment was out of service for an extended period of time before operations personnel identified the condition. ' The two pieces of-equipment involved were the process computer and the radiation monitor recorder.
- Corrective Action:
Concerning the . failure - to identify the unoperability of the process
- computer, an alarm which would have indicated a computer failure was
' inoperative at the time of the computer. failure. This alarm has been returned to service and will be maintained operable. The replacement computer, scheduled for 1986, has full alarm capabilities,for partial or total failures. . To1 prevent a recurrence of this type, control room operators and licensed superviscry personnel have been briefed on the need to frequently monitor computer displays for up-to-date information and how to determine operability status. A logging requirement has been
' incorporated to ensure verification of computer updating. The licensed operators were reminded of the importance of newly licensed personnel tsing a questioning approach to off-normal situations and getting more experienced personnel involved in the investigation as soon as the condition is noted.
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With - respectEtof the1 failure of the- radiation ~ monitor < recorder, the
. Operations DepartmenttStaff havef been instructed and reminded to monitor; key; Control Room instruments for abnormalities and indications -
~
Lof unusual conditions.: In order to ensure that:: activity :is properly
- monitored in accordance with Technical Specifications, the activity levels - !
'being discharged through aerated and clean waste systems is displayed on
' a second redundant recorder which.is' on panel C04. This is recorded-in
- view of the reactor operator at his normal station and could be used as a
,. a: - back-up if the multi-point recorder were to fail in the future. .
I 3' )f Concern: .
On two occasions the unit'was operated at a power level exceeding that permitted b'y Technical Specifications for the method of' monitoring fuel
' rod linear heat rate then in use. One instance involved the loss of the
. computer discussed above.and the.second a-failure to adequately review
. the results of an INCA print out.
Corrective Action:
Refer to item (2) for actions resultant from the March 26, 1983 incident.
- Concerning. the November 4 event, unit engineering procedures were
. revised to require verification that the INCA values are consistent with
- the reactor power level and the reactor engineer provided training for his personnel in this process.
- 4) Concern: -
A series of unplanned or unauthorized releases of radioactive materials on September 16, September 24.and December 28,1982 and' 3anuary 20, 1983, involved common management and personnel errors, particularly
.-lapses in attention to detail and -in first and -second. line management following evolutions. Included were .the discharge' of -the wrong tank .
discharge on a continuous vice.a batch basis, radiation monitor recorder failure during. a discharge and improper valve line-ups. Subsequent performance suggests. that corrective actions were applied piecemeal, conducted informally and without decisiveness and resulted in-little effect.
Corrective Actions: ,
-The referenced unplanned or unauthorized radioactive releases have resulted.in numerous corrective actions;>the most significant are listed below.
(a) Procedure changes to ensure the procedures are accurate and easy-to understand and use for the plant equipment operators have been
. implemented.
- (b) . Instructions to operating personnel have been issued to ensure they l understand the importance and significance of - the events and 1
-necessary corrective actions.
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(c) Requirements to have a second radwaste qualified operator verify l procedure steps for all radioactive discharges in addition to dual 1 verification of valve line-ups for discharges have been' established. -
.-(d) Operations personnel in Unit 2 have been cautioned to critically review all discharges with respect to possible contamination. The ;
sensitivity.of any unplanned radicactive discharge, no matter how slight,~ dictates that stringent controls be used. -
(e) Availability of controlled procedures to radwaste operators has been improved.'
(f} ' Hardware changesj have been accomplished which more clearly identify valves and contr'ols which must be manipulated for-radwaste contiol.
(g) Lastly, an independent review of all Radioactive Waste Operating Procedures and interface procedures (chemistry) was conducted by La Unit 2 senior reactor operator who had not been responsible for-procedural review for radwaste. This review was conducted to ensure usability and compatibility with all other procedures.
Changes from this review were reviewed and implemented.'
- 5) . . Concern:
The quality of services depends greatly on the abilities of the contractor as illustrated by the success of the steam generator sleeving task and the 7 difficulties with.the nozzle' dam installation.
Corrective Action:
NNECO agrees that the quality of the service is dependent on the quality of _the vendor. Therefore, Unit 2 continues to evaluatef all projects performed by~ vendors. . This evaluation is utilized during future vendor selections. Concerning the nozzle dam project, modifications performed on the dams and direct NNECO control of the evaluations resolved the problems with the installation. The 1985 effort was accomplished in' a
. timely manner.
- 6) Concern:
The licensee has not been effective in dealing with the fuel vendor.
Corrective Action: l NUSCO Engineering is in discussion with the fuel vendor to resolve the manufacturing and design problems. Extensive examinations were completed by NNECO, NUSCO and the vendor to identify the failed rods and potential failure mechanisms. A likely mechanism is debris from the thermal shield removal and other primary work. A stringent material inventory control system has been initiated for this refuel to prevent further failures. In addition a full core off-load and fuel sipping is being
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accomplished during the 1985 refueling outage to improve fuel performance for the next operating cycle. The above efforts complement the fuel reconstitution effort which was completed last fall and which was presented to the NRC in a meeting in NRC Bethesda offices on October 3,1984.
- 8) Concern:
The Safety Committee, PORC, conducts most reviews through subcommittees rather than having all members perform the review. This has resulted in a decrease in committee effectiveness in some of its review work.
Corrective Action:
See item 1, corrective action.
- 9) Concern:
A breach of a vital area security boundary was made in the course of a planned facility modification.
Corrective Action:
The breach of the security barrier was a failure of a portion of the PDCR process. A task force on PDCRs has presented recommendations and the recommendations have been implemented. Among these im xovements is a greater consistency during PDCR generation. This and the increased PORC review identified in item I will help prevent future deficiencies of all types from occurring during plant design changes.
Emergency Preparedness See Item 3 for Millstone Unit No.1.
Licensir.g Activities We did not agree with the Category 2 rating in this functional area, for reasons stated in the December 19, 1983 letter to R. W. Starostecki. Accordingly, no significant corrective actions were implemented. It is re-emphasized that the principles and concepts behind our licensing activities for Millstone Unit No. 2 are identical to those applied to the Haddam Neck Plant and Millstone Unit No.1, which were given a Category I rating for this assessment interval.
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