ML19340D382

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RO 2-80-112:on 801209,while Performing Maint on Water Pump Discharge Check Valve,Heatup to Approx 212 F Resulted. STS Change Request Being Considered to Accommodate Similar Maint Needs in Future
ML19340D382
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 12/22/1980
From: Tollison A
CAROLINA POWER & LIGHT CO.
To: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
References
BSEP-80-2106, RO-2-80-112, NUDOCS 8012300472
Download: ML19340D382 (3)


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C@at Carolina Power & Light Company Brunswick Steam Electric Plant P. O. Box 10429 *

Southport, N. C. 28461

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December 22, 1980 -

FILE: B09-13516 .

SERIAL: BSEP/80-2106  ;

1 Mr. James P. O'Reilly, Director U. S. Nuclear Regulatory Commission ,

Region II 101 Marietta Street, Suite 3100 Atlanta, Georgia 30303 BRUNSWICK S, TEAM ELECTRIC PLANT, UNIT NOS. 1 & 2 LICENSE NOS. DPR-71 AND DPR-62 DOCKET NOS. 50-325 AND 50-324 *

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CONFIRMATION OF AN IMMEDIATELY REPORTABLE EVENT (2-80-112) ,

Dear Mr. O'Reilly:

This facimile confirms the conversation between Mr. A. C. Tollison, Jr.,

General Plant Manager, and Mr. Austin Harden of your office of 1630 on December 19, 1980.

While perforning corrective maintenance on 2-SW-V24, 2A Nuclear Service Water pump discharge check valve on December 9,1980, it was necessary to secure all Unit No. 2 service water pumps to completely isolate the valve from pressure. Unit No. 2 was in cold shutdown at the time.

Due to the unexpected duration of this repair, a heatup to approximately 212*F resulted which was reported by RED PHONE and by telephone to Region II. We addressed corrective actions and stated our intention to submit a thirty-day written report.

We have determined, following subsequent review of this incident, that it technically constitutes a prompt nctification event in that STS 3.7.1.2.b requires that core spray, LPCI, and diesels be declared inoperable with less than one service water pump operable. Actually, these systems were operable and available if needed since alternate cooling water was supplied to the diesels.

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Mr. James P. O'Reilly December 22, 1980 We are considering a STS change request to accommodate similar main-tenance needs in the future while, at the same time, assuring adequate core cooling. .

Very truly yours,

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A. C. Toll son, Jr., General Manager .

Brunswick Steam Electric Plant RMP/ACT:sas cc: Mr. R. A. Ilartfield .

Mr. V. Stello, Jr.

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