IR 05000336/2009002

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IR 05000336-09-002, 05000423-09-002; on 01/01/09 - 03/31/09, Millstone Power Station Integrated Inspection Report and Exercise of Enforcement Discretion
ML091340064
Person / Time
Site: Millstone  Dominion icon.png
Issue date: 05/14/2009
From: David Lew
NRC/RGN-I/DRP/PB6
To: Christian D
Dominion Resources
BELLAMY RR
References
EA-09-044, FOIA/PA-2011-0115 IR-09-002
Download: ML091340064 (38)


Text

UNITED STATES NUCLEAR REGULATORY COMMISSION REGION I 475 ALLENDALE ROAD KING OF PRUSSIA, PA 19406-1415 May 14, 2009

EA-09-044

Mr. David Christian

Sr. Vice President and Chief Nuclear Officer

Dominion Resources

5000 Dominion Boulevard

Glen Allen, VA 23060-6711

SUBJECT: MILLSTONE POWER STATION - NRC INTEGRATED INSPECTION REPORT 05000336/2009002 AND 05000423/2009002 AND EXERCISE OF ENFORCEMENT DISCRETION

Dear Mr. Christian:

On March 31, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection

at your Millstone Power Station Unit 2 and Unit 3. The enclosed inspection report documents

the inspection results, which were discussed on April 9, 2009, with Mr. A. J. Jordan and other

members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

This report documents one self-revealing finding of very low safety significance (Green).

Additionally, a licensee-identified violation determined to be of very low safety significance is

listed in the report. However, because of the very low safety significance and because it is

entered into your corrective action program, the NRC is treating the licensee identified violation

as a non-cited violation (NCV) consistent with Section VI.A.1 of the NRC Enforcement Policy. If

you contest any NCV in this report, you should pr ovide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional

Administrator, Region I; the Director, Office of Enforcement, United States Nuclear Regulatory

Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at Millstone.

In addition, the inspectors reviewed Licensee Event Report 50-423/2008-005, which described

the details associated with the failure to maintain 3FWS*V861, "C" steam generator (SG) drain

line isolation valve fully closed. This valve was relied on to meet technical specification (TS)

containment penetration requirements during fuel movement in the Unit 3 containment from

November 1-3, 2008. This was a violation of TS Section 3.9.4.c., which requires each

penetration providing direct access from the containment atmosphere to the environment be closed by an isolation valve, blind flange, or manual valve or be capable of being closed under administrative control during movement of fuel within the containment building. A risk

evaluation was performed and the issue was determined to be of very low safety significance.

Although this issue constitutes a violation of NRC requirements, the NRC determined that the

failure to completely close the valve was not within Dominion's ability to reasonably foresee and

correct, and as a result, the NRC did not identify a performance deficiency associated with this

condition. The NRC's assessment considered that the valve does not have position indication

to provide an alternate means to verify valve position, there were no past condition reports (CR)

documenting difficulty in closing the valve, the work order (WO) documenting "like for like" valve

replacement in 2007 did not indicate difficulty in operating the valve, and Dominion took

corrective action to close the valve and enter the issue into their corrective action process.

Based on the results of the NRC's inspection and assessment, I have been authorized, after

consultation with the Director, Office of Enforcement, and the Regional Administrator, to

exercise enforcement discretion in accordance with Section VII.B.6 of the Enforcement Policy

and refrain from issuing enforcement for this violation.

In accordance with Title 10 of the Code of Federal Regulations (CFR) Part 2.390 of the NRC's

"Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be

available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC's document system (ADAMS).

ADAMS is accessible from the NRC Web Site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,/RA by James W. Clifford Acting For/

David C. Lew, Director

Division of Reactor Projects

Docket Nos. 50-336, 50-423 License Nos. DPR-65, NPF-49

Enclosure:

Inspection Report No. 05000336/2009002 and 05000423/2009002

w/Attachment:

Supplemental Information

cc w/encl: J. Price, Vice President, Engineering, Dominion Fleet

A. Jordan, Site Vice President, Millstone Station

C. Funderburk, Director, Nuclear Licensing and Operations Support

L. Morris, Plant Manager, Millstone Station

W. Bartron, Supervisor, Station Licensing

J. Spence, Manager Nuclear Training

L. Cuoco, Senior Counsel

C. Brinkman, Manager, Washington Nuclear Operations

J. Roy, Director of Operations, Massachus etts Municipal Wholesale Electric Company First Selectmen, Town of Waterford

B. Sheehan, Chair, NEAC

P. Rathbun, Vice-Chair, NEAC

E. Wilds, Jr., Ph.D, Director, State of Connecticut SLO Designee

SUMMARY OF FINDINGS

IR 05000336/2009-002, 05000423/2009-002; January 1, 2009 - March 31, 2009; Millstone

Power Station Unit 2 and Unit 3.

The report covered a three-month period of inspection by resident and region-based inspectors.

Two Green findings were identified. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance

Determination Process." Findings for which the significance determination process (SDP) does not apply may be Green or be assigned a severity level after NRC management review. The

NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.

A. NRC-Identified and Self-Revealing Findings

Cornerstone: Initiating Events

Green.

A self-revealing finding of very low safety significance (Green) was identified for Dominion's failure to control Unit 3 Steam Generator (SG) levels while operating at power. Specifically, Dominion's failure to control SG levels resulted in a reactor trip while reducing power for a plant shutdown. Dominion entered this issue into their corrective action program (CR113512), and corrective actions included conducting just-

in-time (JIT) training on low power feed station operation for licensed operators prior to reactor start up.

This finding is more than minor because it was associated with the Human Performance

Attribute of the Initiating Events cornerstone and affected the cornerstone objective of limiting the likelihood of those events that upset plant stability and challenge critical safety functions during power operations. The inspectors conducted a Phase 1 screening, in accordance with IMC 0609, "Significance Determination Process," and determined that the finding is of very low safety significance (Green) because it did not contribute to both the likelihood of a reactor trip and the likelihood that mitigation equipment or functions would not be available. The inspectors determined that this finding had a cross cutting aspect in the area of Human Performance, Work Control, because Dominion did not coordinate work activi ties, consistent with nuclear safety, by incorporating actions to address the operational impact on control room personnel

[H.3.(b)]. (Section 4OA3.1).

B. Licensee-Identified Violations

One violation of very low safety significance, which was identified by the licensee has been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensee's corrective action program. This violation and corrective actions are listed in Section 4OA7 of this report.

REPORT DETAILS

Summary of Plant Status

Units 2 and 3 operated at or near 100 percent power throughout the inspection period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection

.1 Seasonal Site Inspection

a. Inspection Scope

(1 Sample)

The inspectors reviewed Unit 3's readiness for seasonal cold weather. The inspectors

reviewed applicable procedures and performed walkdowns of the heat tracing, hot water

heating system, and space heaters to verify condition of the weather protection

equipment and determine if they were configured in accordance with Dominion

=s procedures. The inspectors reviewed the Unit 3 Updated Final Safety Analysis Report (UFSAR) and Technical Specifications (TS) and compared the analysis with procedure

requirements to ascertain that procedures were consistent with the UFSAR. The

inspectors performed partial walkdowns of the Unit 3 intake structures, service water (SW) systems, intake structure trav eling screens, and condensate surge and storage tanks to determine the adequacy of equipment protection from the effects of seasonal

cold weather. Documents reviewed during the inspection are listed in the Attachment.

b. Findings

No findings of significance were identified.

.2 External Flooding Inspection

a. Inspection Scope

(1 Sample)

The inspectors evaluated Dominion's protection from the effects of external flooding

conditions at Units 2 and 3. The inspectors reviewed the Final Safety Analysis Report (FSAR) to identify the areas that could be affected by flooding. The inspectors reviewed

applicable procedures to verify that the actions required in the event of flooding could

reasonably be completed. The inspectors conducted a walkdown of the intake

structures and flood doors to determine if the structures were as described in the FSAR

and that the material condition of the structures and components was adequately

maintained. Documents reviewed during the inspection are listed in the Attachment.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment

.1 Partial System Walkdowns

a. Inspection Scope

(4 Samples)

The inspectors performed four partial system walkdowns during this inspection period.

The inspectors reviewed the documents listed in the Attachment to determine the correct

system alignment. The inspectors conducted a walkdown of each system to determine if the critical portions of the selected systems were correctly aligned, in accordance with

the procedures, and to identify any discrepancies that may have had an effect on

operability. The walkdowns included selected switch and valve position checks, and

verification of electrical power to critical components. Finally, the inspectors evaluated

other elements, such as material condition, housekeeping, and component labeling.

The following systems were reviewed based on their risk significance for the given plant

configuration:

Unit 2

Unit 3

b. Findings

No findings of significance were identified.

.2 Complete System Walkdown

a. Inspection Scope

(1 Sample)

The inspectors completed a detailed review of the alignment and condition of the Unit 3

containment recirculation spray system. The inspectors conducted a walkdown of the

"B" train of the system to assess critic al equipment, such as breakers and valves, and were found in good condition and proper alignment in accordance with procedures.

The inspectors also conducted a review of outstanding maintenance work orders (WO)

to determine if any deficiencies could significantly affect system function. In addition, the

inspectors reviewed the system health reports and corrective action database to

determine whether equipment problems were being identified and appropriately

resolved. The inspectors also interview ed the system engineer. Documents reviewed during the inspection are listed in the Attachment.

b. Findings

No findings of significance were identified.

1R05 Fire Protection

.1 Quarterly Fire Protection Walkdowns

a. Inspection Scope

(7 Samples)

The inspectors performed walkdowns of seven fire protection areas. The inspectors

reviewed Dominion's fire protection program to determine the required fire protection

design features, fire area boundaries, and combustible loading requirements for the

selected areas. The inspectors walked down these areas to assess Dominion's control

of transient combustible material and ignition sources. In addition, the inspectors

evaluated the material condition and operational status of fire detection and suppression

capabilities, fire barriers, and any related compensatory measures. The inspectors

compared the existing conditions of the areas to the fire protection program

requirements to determine if all program requirements were being met. Documents

reviewed during the inspection are listed in the Attachment. The fire protection areas

reviewed included:

Unit 2 * "A" and "B" EDG Cubicles 14'-6", Fire Areas A-15/A-16;

  • Auxiliary Building Elevation -25'-6" Fire Area A1, Zones B, E, F;
  • Intake Structure Fire Area I-1, Zones A, B, and C;

Unit 3

  • Auxiliary Building East Floor Area Elevation 24'-6", Fire Area AB-1, Zone C;
  • Auxiliary Building West Floor Area Elevation 24'-6", Fire Area AB-1, Zone D;
  • Control Building West Switchgear Area, Elevation 4'-6", Fire Area CB-1; and
  • Auxiliary Building East and West MCC and Rod Control, Elevation 24'-6", Fire Areas AB-5 and AB-6 Zone A.

b. Findings

No findings of significance were identified.

.2 Annual Fire Drill Observation

a. Inspection Scope

(1 Sample)

Unit 3 The inspectors observed personnel performance during an unannounced fire brigade

drill on March 16, 2009, to evaluate the readiness of station personnel to fight fires. The

drill simulated a fire in the Unit 3 generator exciter and bearing areas. The inspectors

observed the fire brigade members using protective clothing, turnout gear, self-contained

breathing apparatus and entering the fire area. The inspectors also observed the fire

fighting equipment brought to the fire scene to evaluate whether sufficient equipment

was available to effectively control and extinguish the simulated fire. The inspectors

evaluated whether the permanent plant fire hose lines were capable of reaching the fire

area and whether hose usage was adequately simulated. The inspectors observed the

fire fighting directions and communications between fire brigade members. The

inspectors observed the response of control room personnel during the drill. The inspectors also evaluated whether the pre-planned drill scenario was followed and observed the post drill critique to evaluate if the drill objectives were satisfied and that

any drill weaknesses were discussed.

b. Findings

No findings of significance were identified.

1R06 Flood Protection Measures

a. Inspection Scope

(1 Sample)

The inspectors reviewed the flood protection measures for equipment in the Unit 3

Recirculation Spray System (RSS) Rooms. The inspectors evaluated Dominion's

protection of safety-related systems from internal flooding conditions. The inspectors

performed a walkdown of the area, interviewed the system engineer, reviewed the

internal flooding evaluation, and verified that preventive maintenance was being

performed on critical flood protection detection equipment to ensure that equipment and

conditions remained consistent with those indicated in the design basis and flooding

evaluation documents. Documents reviewed during the inspection are listed in the

.

b. Findings

No findings of significance were identified.

1R07 Heat Sink Performance

a. Inspection Scope

(1 Sample)

The inspectors observed the as-found condition of the Unit 3 "B" EDG jacket water

cooler and engine air cooler water heat exchangers after they were opened to verify that

any adverse fouling concerns were appropriately addressed. The inspectors reviewed

the results of the inspections against the acceptance criteria contained within the

procedure to determine whether all acceptance criteria had been satisfied. The

inspectors also reviewed the UFSAR to ensure that heat exchanger inspection results

were consistent with the design basis. Documents reviewed during the inspection are

listed in the Attachment.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program

.1 Resident Inspector Quarterly Review

a. Inspection Scope

(2 Samples)

The inspectors observed simulator-based licensed operator requalification training for

Unit 2 on January 21, 2009, and for Unit 3 on January 27, 2009. The inspectors

evaluated crew performance in the areas of clarity and formality of communications, ability to take timely actions, prioritization, interpretation and verification of alarms, procedure use, control board manipulations, oversight and direction from supervisors, and command and control. Crew performance in these areas was compared to

Dominion management expectations and guidelines as presented in OP-MP-100-1000, A Millstone Operations Guidance and Reference Document.

@ The inspectors compared simulator configurations with actual control board configurations. The inspectors also observed Dominion evaluators discuss identified weaknesses with the crew and/or

individual crew members, as appropriate. Documents reviewed during the inspection

are listed in the Attachment.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

(5 Samples)

The inspectors reviewed five samples of Dominion's evaluation of degraded conditions, involving safety-related structures, systems and/or components for maintenance

effectiveness during this inspection period. The inspectors reviewed Dominion's

implementation of the Maintenance Rule. The inspectors reviewed Dominion

=s ability to identify and address common cause failures, the applicable maintenance rule scoping document for each system, the current classi fication of these systems in accordance with 10 CFR 50.65 (a)(1) or (a)(2), and the adequacy of the performance criteria and

goals established for each system, as appropriate. The inspectors also reviewed recent

system health reports, Condition Reports (CR), apparent cause determinations, functional failure determinations, operating logs, and discussed system performance

with the responsible system engineer. Documents reviewed during the inspection are

listed in the Attachment. The specific systems/components reviewed were:

Unit 2

  • Pressurizer Heaters;

Unit 3

  • Normal Power NSST/RSST; and
  • Engineered Safety Feature (ESF) Load Sequencer.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

(7 Samples)

The inspectors evaluated online risk management for emergent and planned activities.

The inspectors reviewed maintenance risk evaluations, work schedules, and control

room logs to determine if concurrent planned and emergent maintenance or surveillance

activities adversely affected the plant risk already incurred with out of service (OOS)

components. The inspectors evaluated whether Dominion took the necessary steps to

control work activities, minimize the probability of initiating events, and maintain the

functional capability of mitigating systems. The inspectors assessed Dominion

=s risk management actions during plant walkdowns. Documents reviewed during the inspection are listed in the Attachment. The inspectors reviewed the conduct and

adequacy of risk assessments for the following maintenance and testing activities:

Unit 2

  • January 9, 2009, Yellow risk due to "B" EDG, "B" High Pressure Safety Injection (HPSI) OOS, and high trip risk due to environmental factors;

instrument isolation valve to PI-4191);

  • February 18, 2009, Green risk with a high trip risk due to switchyard work, the "A" essential switchgear OOS, the station air compressor OOS and the "F" air compressor OOS;
  • March 26, 2009, Yellow risk due to North Bus Outage high grid risk; Unit 3
  • February 25, 2009, Green Risk impacting "A" Quench Spray System (QSS), Safety Injection (SI), and Residual Heat Removal (RHR) pumps due to maintenance on the

room air conditioning (AC) unit, ACUS1A;

  • February 27, 2009 Emergent repair of 3CHS*CV8152, outboard letdown isolation valve; and
  • March 17 - 20, 2009, failure of normal level control valve 3HDL-LV37B1, resulting in a trip of the "B" heater drain pump and subsequent down power to 90 percent power.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations

a. Inspection Scope

(6 Samples)

The inspectors reviewed operability determinations (OD). The inspectors evaluated the

ODs against the guidance contained in NRC Inspection Manual Part 9900, Technical

Guidance, "Operability Determinations & Functionality Assessments for Resolution of

Degraded or Nonconforming Conditions Adverse to Quality or Safety." The inspectors also discussed the conditions with operators and system and design engineers, as necessary. Documents reviewed during the inspection are listed in the Attachment. The

inspectors reviewed the adequacy of the following evaluations of degraded or

non-conforming conditions:

Unit 2

  • OD 000253 Revision 1, pressurizer proportional heater failure and similar pressurizer back-up heater failures;
  • CR324869, Refueling Water Storage Tank (RWST) cross-tied to non-safety related equipment;
  • CR326558, Floor Drain Covered in the East End of the "A" EDG Room;

Unit 3

  • OD 000248 Rev. 0, Air volume in "B" SIH discharge piping; and

b. Findings

No findings of significance were identified.

1R18 Plant Modifications

a. Inspection Scope

(4 Samples)

To assess the adequacy of the modifications, the inspectors performed walk downs of

selected plant systems and components, interviewed plant staff, and reviewed

applicable documents, including procedures, calculations, modification packages, engineering evaluations, drawings, correctiv e action program documents, the UFSAR, and TS. For the modifications reviewed, the inspectors determined whether selected

attributes (component safety classification, energy requirements supplied by supporting systems, seismic qualification, instrument set points, uncertainty calculations, electrical coordination, electrical loads analysis, and equipment environmental qualification) were

consistent with the design and licensing bases. Design assumptions were reviewed to

verify that they were technically appropriate and consistent with the UFSAR. For each

modification, the 10 CFR 50.59 screenings or safety evaluations were reviewed, as

described in Section 1R02 of this report. The inspectors also verified that procedures, calculations, and the UFSAR were properly updated with revised design information.

In

addition, the inspectors verified that the as-built configuration was accurately reflected in

the design documentation and that post-modification testing was adequate to ensure the

structures, systems, and components would function properly. A listing of documents reviewed is provided in the Attachment. The following modifications were reviewed:

(1) Unit 2 permanent modification, Removal of "A" and "B" Diesel Generator Service Water Inlet Strainer.
(2) Unit 2 temporary modification, re-termination of the power supply of two pressurizer heaters from the back-up electrical supply to the safety related power supply (L106), done to restore the proportional pressurizer heater banks to full capacity

following the failure of two heaters.

(3) Unit 2 temporary modification, temporary leak encapsulation of body to bonnet leak at M22-CN-543, "B" SG feed pump suction vent
(4) Unit 3 temporary modification for Supplemental Heating of the Feedwater Isolation Valve Room was reviewed.

b. Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

(7 Samples)

The inspectors reviewed seven post-maintenance test (PMT) activities to determine

whether the PMT adequately demonstrated that the safety-related function of the

equipment was satisfied, given the scope of the work specified, and that operability of

the system was restored. In addition, the inspectors evaluated the applicable test

acceptance criteria to evaluate consistency with the associated design and licensing

bases, as well as TS requirements. The inspectors also evaluated whether conditions

adverse to quality were entered into the corrective action program for resolution.

Documents reviewed during the inspection are listed in the Attachment. The following

maintenance activities and PMTs were evaluated:

Unit 2 * "A" Emergency Building Filtration System filter replacement on January 30, 2009;

  • Encapsulation of the steam leak on 2-CN-543 condensate vent connection isolation valve on March 6, 2009;

Unit 3

  • Control Building AC Booster Pump 3SWP*P2A motor replacement on January 24, 2009; * "A" SG Feed Line Isolation Valve 3FWS*CTV41A air line repair on February 3, 2009;
  • T/Tavg Channel 4 Calibration on February 6, 2009, following repairs due to channel failure;
  • Stepdown transformer replacement for 120V vital AC bus 3 on February 26, 2009; and
  • Station Black Out (SBO) Diesel maintenance on 3/5/09.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing

a. Inspection Scope

(8 Samples)

The inspectors reviewed eight surveillance activities to determine whether the testing

adequately demonstrated equipment operational readiness and the ability to perform the

intended safety-related function. The inspectors attended pre-job briefings, reviewed

selected prerequisites and precautions to determine if they were met, and observed the

tests to determine whether they were performed in accordance with the procedural

steps. Additionally, the inspectors reviewed the applicable test acceptance criteria to

evaluate consistency with associated design bases, licensing bases, and TS

requirements and that the applicable acceptance criteria were satisfied. The inspectors

also evaluated whether conditions adverse to quality were entered into the corrective

action program for resolution. Documents reviewed during the inspection are listed in

the Attachment. The following surveillance activities were evaluated:

Unit 2

  • SP 2664B and SP 2664C, ""A" and "B" Charging Pump Pulsation Dampener Test,"

Revision 000-02 on February 2, 2009;

  • SP 2605G-008 and SP 2605G-012, "SG Blowdown and Sample Containment Isolation Valve (CIV) Stroke and Timing In Service Testing (IST), Facilities 1 & 2,"

Revision 000-04;

Unit 3

  • SP 3616A.1-016, "Local Operation Test of 3MSS*MOV74A & 3MSS*MOV74C," Rev.

000-03 on January 15, 2009;

  • SP 3712B-001, "Pressurizer Heater Capacity Surveillance Testing," Rev. 006-03 on January 28, 2009;
  • SP 3712NC-001, "Vital Battery Charger Surveillance Load Testing," Rev. 007-01 on January 28, 2009;
  • SP 3622.3-001, "TDAFW Pump Operational Readiness Test," Rev. 014-02 (IST) on January 30, 2009;
  • SP 31002, "Plant Calorimetric," Rev. 010-10 on March 12, 2009.

b. Findings

No findings of significance were identified.

Cornerstone:

Emergency Preparedness (EP)

1EP6 Drill Evaluation

.1 Classification and Notification During Requalification Training

a. Inspection Scope

(1 Sample)

The inspectors reviewed the operator's emergency classification and notification

completed during Unit 3 requalification training on January 27, 2009. The inspectors

verified the classification and notification were accurate and timely.

b. Findings

No findings of significance were identified.

RADIATION SAFETY

Cornerstone:

Occupational Radiation Safety 2OS1 Access to Radiological Significant Areas (71121.01)

a. Inspection Scope

(10 Samples)

During the period February 23 - 26, 2009, the inspectors conducted the following

activities to verify that the licensee was pr operly implementing physi cal, administrative, and engineering controls for access to locked high radiation areas (LHRA), and other

radiological controlled areas (RCA) during normal power operations, and that workers

were adhering to these controls when working in these areas. Implementation of these

controls was reviewed against the criteria contained in 10 CFR 20, relevant to Millstone

Unit 2 and Unit 3 TS and the licensee's procedures.

This activity represents the completion of 10 samples relative to this inspection area, which partially completes the annual inspection requirement of twenty one.

Plant Walkdown and Radiation Work Permit (RWP) Reviews

(1) The inspectors toured accessible RCAs in Unit 2 and Unit 3, and with the assistance of a radiation protection technician, performed independent radiation

surveys of selected areas and components, to confirm the accuracy of survey data, and the adequacy of postings. Plant areas inspected included the Auxiliary

Buildings, Waste Buildings, and Fuel Storage Buildings.

(2) The inspectors identified plant areas where radiological significant work activities were being performed. These activities included making preparations for a Unit 3

spent resin transfer and preparing for transferring high activity Tri-Nuke filters to

a shipping container from the Unit 3 spent fuel pool. The inspectors reviewed the

applicable RWPs and job history files for these activities, to determine if the

radiological controls were acceptable, discussed the status of preparations with

the Unit 3 Radiation Protection Supervisor, and reviewed the electronic

dosimeter dose/dose rate alarm set points to determine if the set points were

consistent with plant policy.

(3) The inspectors determined that there were no current RWPs for airborne radioactivity areas with the potential for individual worker internal exposures to

exceed 50 mrem. The inspectors reviewed the daily quality control checks performed on various airborne counting instruments (SAC-4, BC-4) to confirm that the instruments were operational.

(4) The inspectors determined that during 2008, there were no internal dose assessments for any actual internal exposures that reached the reporting

threshold of greater than 10 mrem Committed Effective Dose Equivalent (CEDE).

The inspectors also reviewed data for the five highest exposed individuals for

2008, the dose/dose rate alarm reports, related CRs, and determined that no

exposure exceeded site administrative, regulatory, or performance indicator criteria. Additionally, the inspectors confirmed that no declared pregnant workers

were employed during 2008.

Problem Identification and Resolution

(5) A review of Nuclear Oversight assessment reports and field observation reports were conducted to determine if dose significant jobs were routinely monitored, radiological protection programs were effectively evaluated, and problems related

to implementing radiological controls were entered into the corrective action

program for resolution.

(6) CRs associated with radiation protection control access that were initiated between October 2008 and February 2009, were reviewed and discussed with

the licensee staff to determine if the follow-up activities were being conducted in

an effective and timely manner, commensurate with their safety significance.

High Radiation Area and Very High Radiation Area Controls

(7) Procedures for controlling access to High Radiation Areas (HRA) and Very High Radiation Areas (VHRA) were reviewed to determine if the administrative and

physical controls were adequate. The inspectors determined that a recently

implemented corporate procedure (RP-AA-201, Access Controls for High and

Very High Radiation Areas), provided additional controls over the replaced site

procedure RPM 5.1.3, that was previously implemented. The inspectors also

evaluated access controls for VHRA areas in Unit 3, by reviewing procedure OP

3361A, "Personnel Access Control to the MID System Components Inside

Containment," and interviewing control room personnel.

(8) Keys to VHRAs stored in the Unit 3 Control Room were inventoried and accessible. LHRAs were verified to be properly secured and posted during plant

tours. Radiation Worker and Radiation Protection Technician Performance

(9) Several radiological related CRs were reviewed to evaluate if the incidents resulted from repetitive worker errors and to determine if an observable pattern

traceable to a similar cause was evident.

(10) The inspectors attended daily Unit 3 Radiation Protection department planning meetings to assess the timeliness of information and level of detail provided to

technicians for ongoing tasks. Radiation Protection Technicians and radworkers were questioned regarding their knowledge of plant radiological conditions and associated controls.

b. Findings

No findings of significance were identified.

2OS2 ALARA Planning and Controls (71121.02)

a. Inspection Scope

(8 Samples)

During the period February 23 - 26, 2009, the inspectors verified that the licensee was

properly implementing operational, engineering, and administrative controls to maintain personnel exposure as low as is reasonably achievable (ALARA) for past activities performed during 2008. Also reviewed were dose controls for current activities and

preparations for the Unit 2 fall (2R19) 2009 refueling outage. Implementation of these

controls was reviewed against the criteria contained in 10 CFR 20, applicable industry

standards, and the licensee's procedures.

Radiological Work Planning

(1) The inspectors reviewed pertinent information regarding cumulative exposure history, current exposure trends, and ongoing activities to assess past 2008

performance and dose challenges for 2009, including the Unit 2 fall refueling

outage (2R19).

(2) The inspectors reviewed the exposure data for tasks performed during 2008 and compared actual exposure with forecasted estimates. Included in this review

were the tasks performed during the Unit 3 (3R12) refueling outage, on-line tasks

performed for both operating units, and Unit 2 dry cask loading/storage

operations.

(3) The inspectors evaluated the departmental interfaces between radiation protection, operations, maintenance crafts, and engineering to identify missing

ALARA program elements and interface problems. The evaluation was

accomplished by reviewing recent ALARA Council meeting minutes, ALARA

Evaluations, departmental dose summaries, attending an ALARA Council

meeting, and interviewing the ALARA coordinator.

The inspectors also reviewed the Radiation Protection Department Continuous

Improvement Initiatives and the 5-year ALARA Plan (2007-2011) that identifies

areas for further improving radiological controls.

Verification of Dose Estimates

(4) The inspectors reviewed the assumptions and basis for the annual 2008 site collective exposure projections for routine power operations and maintenance

activities, and compared the estimated dose with the actual dose received by

workers. The inspectors also reviewed the dose projections for the upcoming

2R19 refueling outage to determine the exposure challenges and preparations

being made for dose significant activities; e.g. thimble tube replacements.

(5) The inspectors reviewed the licensee's procedures associated with monitoring and re-evaluating dose estimates when the forecasted cumulative exposure for

tasks differed from the actual dose received. The inspectors reviewed the

dose/dose rate alarm reports and exposure data for selected individuals

receiving the highest total effective dose equivalent (TEDE) exposures for 2008

to confirm that no individual exposure exceeded the regulatory limit, or met the

performance indicator reporting guideline.

Jobs-In-Progress

(6) The inspectors reviewed the RWPs, associated ALARA Evaluations (AE) and observed various preparations for jobs-in-progress performed at Unit 3, including

transferring spent resin to a shipping cask (RWP3-09-17/AE3-09-02), and

transferring spent Tri-Nuke mechanical filters to a waste disposal container (RWP 3-09-42/AE3-09-10).

(7) The inspectors reviewed recent AEs developed for controlling low dose tasks.

These AEs addressed various Unit 2 maintenance tasks including cleaning tanks

T-20A/B (AE2-09-01), removal of fuel sipping equipment (AE2-09-09), RWST

header vent testing (AE2-09-02), and a Unit 3 containment entry at power to

perform a test on valve 3SIH-V028 (AE3-09-01).

Problem Identification and Resolution

(8) The inspectors reviewed elements of the licensee's corrective action program related to implementing the ALARA program to determine if problems were being

entered into the program for timely resolution. CRs related to controlling

individual personnel exposure and programmatic ALARA challenges were

reviewed.

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES

[OA]

4OA1 Performance Indicator (PI) Verification

.1 Cornerstone: Initiating Events

a. Inspection Scope

(2 Samples)

The inspectors reviewed Dominion submittals for the PIs listed below to verify the

accuracy of the data reported during that period. The PI definitions and guidance

contained in Nuclear Energy Institute (NEI) 99-02, A Regulatory Assessment Indicator Guideline,@ Revision 5, were used to verify the basis for reporting each data element.

The inspectors reviewed portions of the operations logs, monthly operating reports, and Licensee Event Reports (LER) and discussed the methods for compiling and reporting

the PIs with cognizant licensing and engineering personnel. Documents reviewed during

the inspection are listed in the Attachment.

Unit 3

  • RCS Leak Rate from January 1, 2008 to December 31, 2008; and
  • RCS Specific Activity from January 1, 2008 to December 31, 2008.

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems

.1 Review of Items Entered into the Corrective Action Program

a. Inspection Scope

As required by Inspection Procedure 71152, "Identification and Resolution of Problems,"

and in order to help identify repetitive equipment failures or specific human performance

issues for follow-up, the inspectors performed a daily screening of items entered into

Dominion's corrective action program. This was accomplished by reviewing the

description of each new CR and attending daily management review committee

meetings. Documents reviewed during the inspection are listed in the Attachment.

b. Findings

No findings of significance were identified.

.2 Annual Sample

Review of Corrective Actions Related to Simulator Testing and Fidelity

a. Inspection Scope

(1 Sample)

The inspectors performed a focused review of the actions taken and planned in

response to CR-108371 (Documentation of Simulator Testing Not Complete). The

review included a sample of simulator tests that occurred during the period of time from

2006 to 2009 on both units. The inspectors reviewed root cause evaluations, associated

CRs, corrective actions taken, technical evaluations, and planned corrective actions.

The inspectors also interviewed personnel and conducted a walkdown of the Unit 2 and

Unit 3 simulators. Documents reviewed during the inspection are listed in the

.

b. Findings and Observations

No findings of significance were identified.

There were some significant deviations between the Unit 2 and Unit 3 core neutronics

model and the reference plants. The licensee is currently taking credit for initial

licensing reactivity manipulations in the simulator.

The Unit 2 and Unit 3 simulator control banks at 100% power (Unit 2 control bank 7, Unit

3 control bank "D") differential rod worth coefficients were significantly less than the

reference plant values in the upper half of the core. These values did not meet the

requirements of ANS/ANSI-3.5-1998 section 4.1.3.2(1) for normal evolutions. This deviation caused the simulator core temperature response to be less than the reference plant during a rapid downpower maneuver.

This deviation could potentially affect operator response during a rapid plant downpower. This deviation was first identified in

2006 and again in 2008 during Licensed Operator Requalification Inspections. The

corrective action specified was to conduct a training needs assessment. The needs

assessment had not yet been completed as of this inspection cycle. In addition, on Unit

3, control bank "C" integral rod worth was 52% higher, and shutdown bank "A" integral

rod worth was 23% higher than the reference plant. These deviations from ANS/ANSI

3.5-1998 were also documented but were neither corrected nor properly addressed in

the training program.

The Unit 2 simulator normal annual startup test had not been completed for refueling

cycle 2R18. This test was later accomplished for 2R19. Simulator core performance

tests had been completed for the beginning of cycle (BOC) conditions but not for middle

of cycle (MOC) or end of cycle (EOC) conditions for 2R19. When taking credit for

operator licensing reactivity manipulations in the simulator, the core performance fidelity

should be verified for the same or similar conditions under which the manipulations are

being credited.

The Unit 2 simulator response for 4160 VAC breaker closure when synchronizing

between two power sources did not closely match the reference plant response. For

example, while conducting an NRC Job Performance Measure (JPM) in the simulator (paralleling the Unit 2 RSST to the "A" EDG per EOP-2541 "Restoring Electrical Power" 23-H step 9), the operator was required to close breaker A302. Breaker

A302 would not close in the simulator until after the sychroscope pointer was aligned at

the 12:00 position. The procedure explicitly requires the operator to close the breaker

when the sychroscope pointer passes the 11:00 position. If the operator performs the

procedure as written, and releases the breaker prior to reaching the 12:00 position (because the pointer is moving slowly), the breaker will not close. The breaker in the

reference plant will close between the 11:00 and 1:00 positions during the time when the

check relay is activated. The same deviation was identified during previous initial

license training (ILT) and licensed operator requalification training (LORT) exams. The

problem had been the subject of a simulator Discrepancy Report (DR) after the 2005

Unit 2 initial licensing exam but the DR was closed without taking any corrective action

or conducting a training needs assessment.

.3 Annual Sample

Unit 3 Radiation Monitors

a. Inspection Scope

(1 Sample)

The inspectors performed a focused review of the Unit 3 radiation monitors in response

to a number of issues associated with the monitors. The review included equipment

issues from 2007 to 2009. The inspectors interviewed the system engineer, reviewed

system health reports, CRs, associated maintenance rule evaluations and apparent

cause evaluations, the (a)(1) action plan for RE16B, and planned corrective actions.

Documents reviewed during the inspection are listed in the Attachment.

b. Findings and Observations

No findings of significance were identified.

The inspectors identified that failures of maintenance rule performance criteria 105b for radiation monitors that are used to detect a SG tube event were not being tracked.

Specifically, there had been two failures in a 24 month period (criteria is less than four),

neither of which had been recorded. The inspectors also identified that unavailability

hours for performance criteria 1.07 had not been adequately tracked. Specifically, the

system engineer knew that even though the unav ailability hours associated with the loss of both PDP computers did not exceed the performance criteria, the engineer had not

recorded the hours.

4OA3 Follow-up of Events and Notices of Enforcement Discretion

.1 (Closed) LER 05000423/2008002-00, Failure of Four Main Steam Safety Valves to Lift

Within the Acceptance Criteria On October 9 and 10, 2008, with the plant at 100% power, four main steam safety

valves failed to lift within the acceptance criteria (+/-3%) of TS 3.7.1.1. Dominion

attributed the failures to corrosive oxide locking action between surface layer materials

of the disk-seat interface, referred to as "oxide locking". After testing, the safety valves

were adjusted within +/-1% of the TS acceptance criteria. Dominion entered this issue

into their corrective action process CR113238. The inspectors reviewed this LER and

associated CRs. No findings were identified. This failure to comply with TS 3.7.1.1

constitutes a violation of minor significance that is not subject to enforcement action in

accordance with the NRC's Enforcement Policy. This LER is closed.

.2 (Closed) LER 05000423/2008005-00, Containment Penetration Not Fully Closed During

Fuel Movement On November 5, 2008, with the plant in Mode 6, operators discovered that 3FWS*V861, "C" SG drain line isolation valve, which was relied on to meet TS containment

penetration requirements during fuel movement in containment, was not fully closed. TS 3.9.4.c requires that each penetration providing direct access from the containment

atmosphere to the environment be closed by an isolation valve, blind flange, or manual valve or be capable of being closed under administrative control during movement of fuel

within the containment building. Dominion's investigation subsequently determined that

the valve had been in this condition during fuel movements inside containment from

0430 on November 1, 2008 until 0915 on November 3, 2008. Operators identified that

the valve was leaking while filling the "C" SG on November 5, 2008. They attempted to

close the valve and were not successful until mechanical leverage was applied.

The inspectors reviewed the LER and Dominion's apparent cause evaluation of the

event. The inspectors determined that the failure to completely close valve 3FWS*V861

was not within Dominion's ability to foresee and correct and was not a performance

deficiency. Valve 3FWS*V861 does not have position indication. The operator who

closed the valve and the operator who performed the independent verification did not

have an alternate means to verify that the valve was completely closed. Additionally, when the valve was identified to be leaking while filling the SG, it was only able to be

completely closed when mechanical leverage was applied. A review of previous work

orders (WOs) revealed that the valve was replaced "like for like" in 2007 due to seat

leakage. A different packing was used which required more force to consolidate. Also, the packing gland was torqued per procedure when, previously, the packing was

tightened using "good mechanical practices." Because of these changes, more force would be required to operate the valve; however, there was no indication in the 2007 WO that the valve was difficult to operate. A review of the CRs associated with this

valve did not indicate any previous problems in operating the valve. Because of these details, the inspectors concluded that the inability to fully close valve 3FWS*V861 could

not have reasonably been avoided or detected by Dominion's quality assurance program

or other related control measures. The inspectors also performed a Phase1 SDP

analysis and determined the violation to be of very low safety significance (Green).

Dominion's corrective actions included closing the valve, entering the issue into their

corrective action process (CR 117527), changing the position verification procedure to

specify physical verification versus visual, and plans to modify the valve during the next refueling outage to improve the stroking function. Therefore, in accordance with Section

VII.B.6 of the Enforcement Policy, the NRC has chosen to exercise enforcement

discretion and not issue a violation for this issue. This LER is closed.

.3 (Closed) LER 05000423/2008003-00, Automatic Reactor Trip During Shutdown for

Refueling Outage 3R12 On October 11, 2008, Unit 3 received an automatic reactor trip at approximately 30%

power, while the unit was reducing power in preparation for a refueling outage. The

control room operators were in manual control of the feedwater system. The plant was

experiencing SG level oscillations as a resu lt of removing feedwater system components from service. Oscillations increased and the "A" SG reached its high-high setpoint, resulting in an automatic turbine trip and feedwater isolation. "C" and "D" SG levels

shrank to their low-low level setpoint which caused an automatic reactor trip.

The inspectors witnessed Unit 3's reactor trip and observed plant response and operator

actions in order to evaluate the performance of the mitigating systems and the control

room operators. The inspectors also reviewed the post trip review report and root cause

evaluation. Documents reviewed during the inspection are listed in the Attachment.

Introduction

A self-revealing finding of very low safety significance (Green) was identified for Dominion's failure to control Unit 3 SG levels while operating at power.

Specifically, Dominion's failure to control SG levels resulted in a reactor trip while

reducing power in preparation for a plant shutdown.

Description

On October 11, 2008, Millstone Unit 3 was reducing power in preparation for its 12 th refueling outage. An operator was stationed at main board 5 to remove the "A" Turbine Driven Feedwater Pump (TDFWP) from service when power was less than

50%. The operator remained in place and responded to numerous SG level oscillations.

TDFWP speed was raised out of the normal range to increase differential pressure (DP)

across the feedwater regulating valves (FRVs) because the operator believed this would

assist in controlling the level oscillations.

Another operator noticed the high DP and brought it to the attention of the unit

supervisor. The unit supervisor stationed this operator at the feed station to restore feed

to steam DP to normal. The operator lowered feed pump speed which caused the FRVs

to open in order to maintain the same flow. As the FRVs opened, feed header pressure

dropped and the operator increased feed pump speed to recover DP. This sent a large

amount of relatively cold water to the SGs before the FRVs could be closed. As the

water in the SGs expanded due to heating, levels in the "A" and "B" SGs reached the

high-high setpoint. This caused a turbine trip and feedwater isolation. "C" and "D" SGs

shrank to the low-low level setpoint, resulting in an automatic reactor trip.

Dominion's root cause evaluation determined that the organization, with respect to monitoring and measuring crew performance, was not effective in implementing programs designed to manage challenges to the operators during a plant shutdown.

While the organization was aware of the challenges in manually operating the feed

station, it did not identify the need to improve the feed station's overall performance via

the corrective action process. Additionally, a decrease in proficiency in manual feed

station operation at low power levels was not identified, lower power feed station

operation was not covered in JIT training, and the feed station operator had not received

JIT training. The root cause evaluation also determined that inadequate rigor for outage

preparation expectations resulted in Operations being challenged prior to and during the

shutdown. Also, the control room operators were distracted by numerous tagging-

related shutdown activities during the shutdown.

Analysis:

The inspectors determined that Dominion's failure to maintain control of Unit 3 SG levels was a performance deficiency. Specifically, the failure to control SG levels

resulted in a reactor trip while reducing power in preparation for a plant shutdown.

Traditional enforcement does not apply because there were no actual safety

consequences, impacts on the NRC's ability to perform its regulatory function, or willful

aspects of the finding.

This finding is more than minor because it was associated with the Human Performance

Attribute of the Initiating Events cornerstone and affected the cornerstone objective of

limiting the likelihood of those events that upset plant stability and challenge critical

safety functions during power operations. Specifically, Dominion's failure to control SG

levels resulted in an automatic reactor trip while reducing power in preparation for a

plant shutdown. The inspectors conducted a Phase 1 screening, in accordance with

IMC 0609, "Significance Determination Process," and determined that the finding is of

very low safety significance (Green) because it did not contribute to both the likelihood of

a reactor trip and the likelihood that mitigation equipment or functions would not be

available.

The inspectors determined that this finding had a cross cutting aspect in the area of

Human Performance, Work Control, because Dominion did not coordinate work

activities, consistent with nuclear safety, by incorporating actions to address the

operational impact on control room personnel [H.3.(b)].

Enforcement

No violation of regulatory requirements occurred, because the main feed pumps, feed regulating and bypass valves, and SG level control system are not safety-related. Because this finding does not involve a violation of regulatory requirements and

has very low safety significance, it is identified as a finding. Dominion entered this issue

into their corrective action program (CR113512) and corrective actions included

conducting training in low power feed station operation for licensed operators prior to reactor start up. (FIN 05000423/2009002-01, Failure to Control Steam Generator Water Levels Results in Automatic Reactor Trip)

.4 (Closed) LER 05000423/2008006-00, Turbine-Driven Auxiliary Feedwater Pump Steam

Trap Isolation Valves Found Closed On November 24, 2008, Dominion determined that at 0025, with the plant at 18% power, Unit 3 control room operators identified that the TDAFW pump steam trap isolation

valves were closed. The TDAFW pump was declared inoperable and Technical Specification Action Statement (TSAS) 3.7.1.2.c was entered. The valves were promptly opened, steam traps blown down, the TDAFW pump restored to operable status and the

TSAS exited at 0346. Dominion's investigation determined that the valves were

inoperable since November 22, 2008 at 1746, a total of 34 hours3.935185e-4 days <br />0.00944 hours <br />5.621693e-5 weeks <br />1.2937e-5 months <br />. During this 34 hour3.935185e-4 days <br />0.00944 hours <br />5.621693e-5 weeks <br />1.2937e-5 months <br />

period, the unit went through two mode changes (Mode 3 to Mode 1). This licensee-

identified finding is a violation of TS 3.0.4 which in part requires that the TDAFW pump

be operable prior to changing operational modes. The enforcement aspects of this

finding are discussed in Section 4OA7. This LER is closed.

4OA5 Other Activities

.1 World Association of Nuclear Operators (WANO) Peer Review Report.

a. Inspection Scope

(1 Sample)

The inspectors reviewed the report for the WANO plant assessment of Millstone Nuclear

Generating Station conducted June 2008. The inspectors reviewed the report to ensure

that issues identified were consistent with the NRC perspectives of Millstone

performance and to verify that the WANO team did not identify any safety significant issues requiring further NRC follow-up.

b. Findings

No findings of significance were identified.

4OA6 Meetings, including Exit

Exit Meeting Summary

On April 9, 2009, the resident inspectors presented the overall inspection results to Mr.

A. J. Jordan, and members of his staff. The inspectors confirmed that no proprietary

information was provided or examined during the inspection.

4OA7 Licensee Identified Violations

The following violation of very low safety significance (Green) or Severity Level IV was

identified by the licensee and is a violation of NRC requirements which meets the criteria

of the NRC Enforcement Policy for being dispositioned as a Non-Cited Violation (NCV).

TS 3.0.4 states, in part, that entry into an operational mode shall not be made when the

conditions for the Limiting Condition for Operation are not met and the associated action

requires a shutdown if they are not met within a specified time interval. Contrary to this, from November 22, 2008 at 17:46 until November 24, 2008 at 03:46, Unit 3 did not meet

the conditions for TS 3.7.1.2, AFW system due to an isolated steam trap, and

transitioned from mode 3 to mode 1. Dominion restored the AFW system to operability

and entered the issue into their corrective action process, CR120030. This finding is of

very low safety significance because the findi ng does not involve a loss of system safety function or a loss of safety functions of a single train for greater than its TS allowed

outage time.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee personnel

G. Auria Nuclear Chemistry Supervisor

B. Bartron Supervisor, Licensing
P. Baumann Manager, Security
C. Chapin Supervisor, Nuclear Shift Operations Unit 2
A. Chyra Nuclear Engineer, PRA

T. Cleary Licensing Engineer

G. Closius Licensing Engineer

L. Crone Supervisor, Nuclear Chemistry

J. Dorosky Health Physicist III

M. Finnegan Supervisor, Health Physics, ISFSI
R. Griffin Director, Nuclear Station Safety & Licensing
W. Gorman Supervisor, Instrumentation & Control

J. Grogan Assistant Operations Manager

C. Houska I&C Technician

A. Jordan Site Vice President

J. Kunze Supervisor, Nuclear Operations Support
B. Krauth Licensing, Nuclear Technology Specialist
J. Laine Manager, Radiation Protection/Chemistry
B. Barron Manager, Nuclear Oversight
P. Luckey Manager, Emergency Preparedness
R. MacManus Director, Engineering
M. O'Connor Manager, Engineering

L. Morris Plant Manager

M. Roche Senior Nuclear Chemistry Technician

J. Semancik Manager, Operations

A. Smith Asset Management

S. Smith Supervisor, Nuclear Shift Operations Unit 3
J. Spence Manager, Training
S. Turowski Supervisor, Health Physics Technical Services
C. Vournazos IT Specialist, Meteorological Data

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

Closed

05000423/LER-2008-002-00 LER Failure of Four Main Steam Safety Valves to Lift Within the
Acceptance Criteria (Section 4OA3).
05000423/LER-2008-003-00 LER Automatic Reactor Trip During Shutdown for Refueling
Attachment
Outage 3R12 (Section 4OA3).
05000423/LER-2008-005-00 LER Containment Penetration Not Fully Closed During Fuel
Movement (Section 4OA3).
05000423/LER-2008-006-00 LER Turbine-Driven Auxiliary Feedwater Pump Steam Trap
Isolation Valves Found Closed (Section 4OA3).
BASELINE INSPECTION PROCEDURE PERFORMED
71121.01 Access Controls to Radiological Significant Areas 2OS1
71121.02 ALARA Planning and Controls 2OS2

LIST OF DOCUMENTS REVIEWED

Section 1R01: Adverse Weather Protection

AOP 2560,"Storms, High Winds and High Tides," Rev. 010-04
AOP 3569, "Severe Weather Conditions'" Rev. 016-00
C
OP 200.13, "Cold Weather Preparations," Rev. 002-02
DM2-00-0389-06, "Modification to MP2 EDG Security Gate and Flood Door Sill Installation"
MP 2721C, "Protection and Restoration of Service Water Pump Motor During a PMH," Rev.
007-02
OP 3314G, "Intake Structure Ventilation," Rev. 009-06
OP 3331B, "Plant Heating," Rev. 011-04
OP 3352, "Heat Tracing," Rev. 013-03
SP 2665, "Building Flood Gate Inspections," Rev. 005-05
2341A - Fire Doors and Barriers System Health Report 4

th Quarter 2008

M2 07 03237
CR121295
CR318618
CR318654
CR326339

Section 1R04: Equipment Alignment

OP 3322, "Auxiliary Feedwater Train A," Revision 006
DWG No. 25212-26390 sheet 2
OP 3326-01, "Train A Service Water System," Rev. 009-03
OP 3326-02, "Train B Service Water System," Rev. 009-03
OP 3326-03, "RPCCW A Service Water System Supply," Rev. 004-01
OP 3326-09, "Service Water System - Control Building Air Cond "A" Supply," Rev. 007
OP 3326-18, "MCC and Rod Control Area A/C A Service Water System Supply," Rev. 007-01
OP 3326-23, "Service Water Electrical Checklist," Rev. 007-03
OP 3346A-001, "EDG A - Cooling Water Valve Lineup," Rev. 007
OP 3346A-002, "EDG B - Cooling Water Valve Lineup," Rev. 007
OP 3346A-003, "EDG A - Lube Oil Valve Lineup," Rev. 006-01
OP 3346A-004, "EDG B - Lube Oil Valve Lineup," Rev. 006-01
OP 3346A-005, "EDG A - Starting Air Valve Lineup," Rev. 008-02
OP 3346A-006, "EDG B - Starting Air Valve Lineup," Rev. 009-02
OP 3346A-007, "EDG A - Crankcase Vacuum Valve Lineup," Rev. 005
Attachment
OP 3346A-008, "EDG B - Crankcase Vacuum Valve Lineup," Rev. 005
OP 3346A-009, "EDG A - Instrument Valve Lineup," Rev. 006-01
OP 3346A-010, "EDG B - Instrument Valve Lineup," Rev. 007-01
OP 3346A-011, "EDG A - Electrical Lineup," Rev. 009
MP-20-WP-GDL20 Attachment 15.1, "Scaffo ld Evaluation for WO53102186740 Unit 2 "B" EDG

Section 1R05: Fire Protection

Millstone Unit 2 Firefighting Strategies, April 2002
Millstone Unit 3 Firefighting Strategies, April 2002
Millstone Unit 3 Nuclear Power Station Fire Protection Evaluation Report, Rev. 16
203-SP-M2-SU-1046 Rev 00, Millstone Unit 2 Appendix "R" Compliance Report

Section 1R06: Flood Protection Measures

Millstone Unit 3 Internal Flooding Evaluation Reactor Plant Aerated Drains (contaminated) System Health Report 4

th quarter 2007 and 2008

DCR M3-97079, "Containment Recirculation Cubicle Sumps 3DAS-SUMP7A/B Design
Change," Rev. 1
M3-EV-08-0029, "Technical Evaluation for DAS System and ECCS Limited Passive Failure
Design Criteria/EQ Program Switch Submergence," Rev. 3
M3-EV-970281, "Technical Evaluation for ECCS Passive Failure Design Criteria," Rev. 3
M3 05 15754
M3 06 02859

Section 1R07: Heat Sink Performance

EN 31084, "Operating Strategy for Service Wa ter System at Millstone Unit 3," Rev. 007
Service Water Cooled Heat Exchangers Inspection Forms for "B" EDG Heat Exchangers,
3EGS*E1B and 3EGS*E2B
CR323008

Section 1R11: Licensed Operator Requalification Program

Unit 2 LORT Operating Exercise #2, Degraded Voltage
MP3 LOIT/LORT, LORT SE46, Rev. 2
OP-MP-100-1000, A Millstone Operations Guidance and Reference Document.

@

Section 1R12: Maintenance Effectiveness

C
PT 1402, "Timing Device Calibration," Rev. 001-03, performed August 14, 2006
C
PT 1407, "Panel Meter and Transducer Calibration," Rev. 001-04, performed August 15, 2006
C
PT 1410, "5kV and 8kV Cable Tests," Rev.001-03, performed April 25, 2007
C
PT 1425 B4, "Relay Type BDD18B Transformer Di fferential," Rev. 1, performed November 3, 2008
M2-EV-01-0006, "Technical Evaluation for EDG Availability During Testing," Rev. 02
MP2-ENG-ETAP-04014E2, "MP2 Electrical Distribution system Analysis," Rev. 1
OP 3346C, "EGLS Individual Load Testing," Rev. 005-01
PT 31412K1, "MP3 15G-3SA (4.16KV NSST) Test," Rev.001-02, performed October 30, 2008
PT 31460A, "MO3
RSST-B, 6.9 KV Non-segregated Bus Test," Rev.002-01, performed August
17, 2006
SP 3646A.16-001, "Train B Loss of Power Test," Rev. 013-01
SP 3646A.16-002, "Train B Loss of Power Test Failure and Retest Documentation," Rev. 006
SP 3646A.18-002, "Train B ESF with LOP Test Failure and Retest Documentation," Rev. 006
Attachment
EDG 2346A, B Unavailability March 2007 to February 2009
EDG and Fuel Oil System, 2346A, B System Health Report 4

th Quarter 2007, 2008

Eng'd Safeguards Actuation Sys (Sequencer), 3405, System Health Report, 4

th quarter 2007

and 2008

ESF Load Sequencer Unavailability 2007-2008
MRule (a)(1) Evaluation for the Normal Power System (2347),
CR-08-06119, Rev. 00
MRule (a)(1) Evaluation for the Normal Power System (2347),
CR-08-06209, Rev. 00
MRule (a)(1) Evaluation for the Normal Power System (3347),
CR-07-04550, Rev. 00
MRule (a)(1) Evaluation for the Emergency Generator Loading Sequencer (3405), CR-07-
208, Rev. 0
MRule Functional Failure Evaluations Evaluation for Unit 2 Pressurizer Proportional Heaters

(07137),

CR114357 Maintenance Rule Functional Failure Evaluations,
CR-07-03270,
CR-07-04550,
CR-07-05208,
CR-08-01476,
CR-08-04403,
CR-08-05611,
CR-08-07480,
CR118400
Maintenance Rule Functional Failure Evaluations for Unit 2 EDGs,
CR-07-02244,
CR-07-03568,
CR-07-06155,
CR-07-06624,
CR-07-11454,
CR-08-00303,
CR-08-00305,
CR-08-00329, CR-
08-00330
Maintenance Rule Functional Failure Evaluations for Unit 2 RSST,
CR-08-04050,
CR-08-04269,
CR-08-06119,
CR-08-06265
NSST, RSST, Main Transformers, and Isophase Bus System Health Reports, 3347A, B, C, 4

th quarter 2007, 2

nd , 3 rd , and 4 th quarter 2008

NSST Unavailability 2007-2008
ODM for
CR-08-06265
RSST, 2347A Fluid Analysis Report for Dissolved Gases 2008, 2009
RSST, 2347A System Health Report 4

th Quarter 2007 and 2008

RSST 2347A, Unavailability 2007-2008
RSST 3347A, Unavailability 2007-2008
CR-06-00052
CR-06-01467
CR-07-04618
CR-07-06624
CR-07-07782
CR-07-08147
CR-07-08550
CR-07-12481
CR-08-00912
CR-08-06613
CR-08-07109
CR-08-08370
CR118400
CR322051
MRE006987
MRE007244
MRE007358
MRE010264
MRE010309

Section 1R13: Maintenance Risk Assessments and Emergent Work Control

DCN
DM2-00-0043-09, "Leak Sealant Repair of Valve 2-MS-440" Attachment
NF-AA-PRA-370, "Probabilistic Risk Assessment Procedures and Methods:
PRA Guidance for
MRule (a)(4)," Rev. 0
North Bus Outage Implementation Plan, Rev. 0
WM-AA-100, "Work Management," Rev. 4
CR323435

Section 1R15: Operability Evaluations

DCN
DM2-01-0212-07 Replacement of Spool P24 to the "B" EDG Strainer
EE-99032, "Maximum Allowable Gas Bubble Size at ECCS High Points," Rev. 02
IOD 000147 Rev. 0, 3SIH*V28 was replaced and field weld 43 did not have the required NDE

performed

IOD000149 Rev. 0, Air volume in "B" SIH discharge piping
M3-EV-05-0008, "Determination of Allowable ECCS Gas Accumulations in Support of
Surveillance 4.5.2.b.1," Rev. 2
MP-VE-9, "Visual Weld Acceptance Criteria for Weldments and Braze Joints," Rev. 000
53M30800403
NUCENG-07-048, "Evaluation of Gas Voids in MP3 SIH Discharge Piping," Rev. 4
203-ER-08-0005 MP2 EDG Floor Drain Backwater Valves
Tech Eval M2-EV-01-0006 "EDG Availability during Testing"
MRE07137 "Pressurizer heater 3RCS*HTR48 has faulted"
MRE10244 "Group 2 Proportional heater Reduced Capacity"
IOD 000150 "Unit 2 Group 2 Pressurizer Heater Capacity Less than Normal"
CR114357
CR318967
CR318997
CR319295
CR319371
CR320282
CR324239
CR324869
CR326019
CR326558

Section 1R18: Plant Modifications

C
OP 200.13, "Cold Weather Preparations," Rev. 002-02
SP 3621.1, "Main Feedwater Valve Operability Test," Rev. 010-02
WC 10, "Temporary Modifications," Rev. 005-07
Temporary Log dated 1/1/09 Feedwater Isolation Valve Temperatures
DM-2-00-0054-08 "Removal of "A" and "B" EDG Service Water Inlet Strainer"
MP58B-00138EM, Rev 3 "Service Water Supply to Diesel Engine Coolers"
CCN-22
OP-2346A Rev 27-04 "A" EDG
ARP-2591A Rev 004-01 "Alarm Response for "A" DG Panel, C-38"
50.59 Screen Removal of "A" and "B" EDG Service Water Inlet Strainer
50.59 Screen Supplemental Heating for FWIV Room
DCN:
DM2-00-0014-09
50.59/72.48 Screen for
DN2-00-0014-09
DCN:
DM2-00-0064-09 "Temporary Leak Encapsulation on Body to Bonnet Leak at
M22-CN-543 "B" SGFP Suction Vent"
Calc# PIPEWHIP -1802M2 Rev 2, "Assessment of Pipe Whip Restraints, Millstone Unit 2" Attachment Calculation Change Notice PIPEWHIP-1802M2 Rev 2
Vendor Calc# Bechtel
PR-L Rev 1, "Main Feedwater Restraint
MFR 16 and
MFR 16"
CR119948
CR119953
CR119959
CR317924
CR325093

Section 1R19: Post Maintenance Testing

Bechtel Calculation#
PR-L "Main Feedwater Pipe Restraint
MFR 15 and
MFR 16" Rev 1
DCR M3-06004, "Unit 3 Vital Inverters Replacement", Rev. 0
DCN
DM2-00-0064-09 "Temporary Leak Encapsulation of Body to Bonnet Leak at M22-CN-543

"B" SGFP Suction Vent Valve"

DM3-00-0027-07, "MP3 Vital Inverter Replacement," Rev. 07
MP 3760DB, "SG FWIV - Hydraulic Fluid and N2 Levels," Rev. 008-01
OP 3346D, "Station Blackout Diesel," Rev. 011-05
Calc # PIPEWHIP-1802M "Assessment of Whip Restraints, Millstone Unit 2" Rev 2 and CCN 1
SP 3442A40-001, "T/Tavg Channel 4 Calibration Data Sheet," Rev. 013-06
SP 3443D21-001, "Protection Set Cabinet IV Operational Test Data Sheet," Rev 018-07
SP 3626.8-001, "Control Building Air Conditioning Booster Pump 3SWP*P2A Operational Test"
SP 3670.4-015, "Quarterly SBO PM," Rev. 001-04
Readiness Test," Rev. 010-06"
M3 07 00922
53102177167
53M30406863
53M30711915
53M30713534
53M30713536
53M30808635
CR325093
CR325463
CR325558
CR325591

Section 1R22: Surveillance Testing

SP 3601F.6-001, "RCS Inventory Balance," Rev. 002-04
Section 2OS1/2OS2:
Access to Radiologically Significant Areas/ALARA Planning and Controls Procedures
RPM 1.3.8, Rev 8, Criteria for Dosimetry Issue
RPM 1.3.13, Rev 9, Bioassay Sampling and Analysis
RPM 1.3.14, Rev 8, Personnel Dose Calculations and Assessments
RPM 1.4.1, Rev 8, ALARA Reviews and Reports
RPM 1.4.2, Rev 2, ALARA Engineering Controls
RPM 1.6.4, Rev 4, Siemens Electronic Dosimetry System
RPM 2.1.1, Rev 7, Issuance and Control of RWPs
RPM 2.1.2, Rev 2, ALARA Interface with the RWP Process
RPM 2.1.3, Rev 2, Identification and Control of High Radiological Risk Work Attachment
RPM 5.2.2, Rev 13, Basic Radiation Worker Responsibilities
RPM 5.2.3, Rev 3, ALARA Program and Policy
RPM-GDL-008, Rev 0, Electronic Dosimeter Alarm Set Points
RP-AA-201, Rev 2, Access Controls for High and Very High Radiation Areas
RP-AA-202, Rev 0, Radiological Posting
RP-AA-220, Rev 0, Radiological Survey Scheduling
RP-AA-221, Rev 0, Radiological Survey Records
RP-AA-222, Rev 0, Radiation Surveys
RP-AA-226, Rev 0, Airborne Activity Surveys
RP-AA-230, Rev 0, Personnel Contamination Monitoring and Decontamination
OP 3316A, Rev 8, Personnel Access Control to the MID System Components Inside Containment
Quality Assurance Reports Field Observation Report Nos. 9108, 9140, 9201, 9338, 9345, 9212, 8744, 8746, 8737, 8780,09-005, 09-
2,08-052, 08-051,08-045, 08-046,08-048
Self Assessment Report
SAR 000819, High Radiation Area (HRA) & Locked High Radiation Area (LHRA) Controls, Gap Analysis

Condition Reports

(Access Controls/ALARA)

116937,
114914,
117796,
317011,
117550,
321230, 322470-1,
317349
ALARA Evaluation Numbers
2-09-01, 02-09-02, 02-09-09, 03-09-03, 03-09-10
ALARA Council Meeting Minutes Meeting Dates: 02/26/2009, 12/18/2008, 09/17/2008

Miscellaneous

Dose and Dose Rate Alarm Reports for October 2008 through January 2009
MP2 Thimble Replacement Overview
Ten Highest Doses received during 2008
3R12 Post Outage Report
Radiation Protection Top Focus Items for 2009
2R19 3" Spray Line Cut and Replace Risk Evaluation

Section 4OA1: Performance Indicator (PI) Verification

CP 3807F, "Operation of the Reactor Plant Sample Sink," Rev. 004-09
SP 3601F.6, "Reactor Coolant System Water Inventory Measurement," Rev 005-06
SP 3670.1, "Mode 1-4 Daily and Shiftly Control Room Rounds," for March, September, and
December 2008
SP 3855, "Reactor Coolant Analysis for Dose Equivalent I-131," Rev. 007
SP 3855-001, "Reactor Coolant Analysis for Dose Equivalent I-131," Rev. 007-01
Dose Equivalent Iodine Spreadsheet, 2008
Unit 3 Quantitative Radioisotopic Iodine Analysis February 2008 and September 2008
RCS Leakage Spreadsheet 2008

Section 4OA2: Identification and Resolution of Problems

Attachment Simulator Testing
NSEM-4.07, "Nuclear Simulator Engineering Manual, Master Testing Schedule"
MP2 Simulator Recovery Plan
RCE108505, "Discrepancies Exit with Unit 2 Simulator Testing Records"
Unit 2 Simulator Core Performance Test Cycle 19 2008 (all CPTs)
Unit 2 Scenario Based Testing ES08101a, "SGTL, SGTR with Complications" and SO8202,

"Plant Heatup and Termination of Shutdown Cooling" dated 2/20/2008

Unit 2 Simulator Transient Tests: T1, "Manual Reactor Trip" dated 11/5/2008, and T4,

"Simultaneous Trip of all RCPs" dated 11/5/2008

Unit 2 Simulator Steady State Tests Stability Test 100% Power dated 9/10/2008
Internal Assessment 2008-01 dated 9/19/2008
Internal Assessment 2008-05
Unit 3 Simulator Core Performance Tests Cycle 13 (all CPTs)
CR-07-08202
CR-08-06997
CR108371
CR108505
CR108838
CR109159
CR109817
CR111110
CR324101
CR324772
CR325250
CR325305
CR325584
CR325620
CR327009
CR327201
CR327592
CR328186
Unit 3 Radiation Monitors Maintenance Rule (a)(1) Action Plan for RE16B,
CR107039
Maintenance Rule Evaluations for the following CRs:
CR-07-04412,
CR-07-04977, CR-07-
05812,
CR-07-09317,
CR-7-10934,
CR-07-11455,
CR-08-00432,
CR-08-00671,
CR-08-02554,
CR-08-02759,
CR-08-02782,
CR-08-03343
Maintenance Rule Scoping Tables for Radiation Monitors, 3404
Radiation Monitoring, 3404 System Health Report 4

th quarter 2007 and 2008

ACE013937
ACE017322
CR-07-00577
CR-07-02356
CR-07-02703
CR-07-05966
CR-07-06024
CR-07-06631
CR-07-07753
Attachment
CR-07-11132
CR-07-11583
CR-08-00188
CR-08-00567
CR-08-02191
CR-08-02201
CR-08-02226
CR-08-02467
CR-08-04517
CR107011
CR120626
CR326590
MRE006964
MRE007117
MRE007126
MRE007237
MRE007360
MRE010152
MRE010237
MRE010250
MRE010263
MRE010267

Section 4OA3: Followup of Events

CR113238 CR118282

Section 4OA5: Other Activities

WANO Peer Review Report

LIST OF ACRONYMS

AC Alternating Current

ADAMS Agencywide Documents

Access and Management System

AE [[]]
ALARA Evaluation
AFW Auxiliary Feedwater
ALARA As Low as Reasonably Achievable
ASME American Society of Mechanical Engineers
BOC Beginning of Cycle
CEDE Committed Effective Dose Equivalent
CFR Code of Federal Regulations
CIV Containment Isolation Valve
CLB Current Licensing Basis
CR Condition Report
DNB Departure from Nucleate Boiling
DNC Dominion Nuclear Connecticut
DP Differential Pressure
DR Discrepancy Report

DRP Division of Reactor Projects

Attachment

DRS Division of Reactor Safety
ECCS Emergency Core Cooling System
EDG Emergency Diesel Generator
EOC End of Cycle
EP Emergency Preparedness
ESF Engineered Safety Feature
FRV Feedwater Regulating Valves
FSAR Final Safety Analysis Report
HPSI High Pressure Safety Injection
HRA High Radiation Areas
JIT Just-in-Time
JPM Job Performance Measure
I&C Instrumentation and Control
ILT Initial License Training
IMC Inspection Manual Chapter
IST In Service Training
JPM Job Performance Measures
LER Licensee Event Reports
LHRA Locked High Radiation Areas
LORT Licensed Operation Requalification Training
MCC Motor Control Center

MOC Middle of Cycle

mrem millirem

NCV Non-Cited Violation
NDE Non-Destructive Examination
NEI Nuclear Energy Institute
NRC Nuclear Regulatory Commission
OA Other Activities
OD Operability Determinations
OOS Out Of Service
PARS Publicly Available Records System
PI Performance Indicator
PI&R Problem Identification and Resolution
PM Preventive Maintenance
PMT Post Maintenance Testing
QSS Quench Spray System
RCA Radiologically Controlled Area
RCS Reactor Coolant System
RHR Residual Heat Removal
RO Reactor Operator
RPS Reactor Protection System
RSS Recirculation Spray System
RSST Reserve Station Service Transformer
RWP Radiological Work Permit
RWST Refueling Water Storage Tank
SBO Station Black Out
SBT Scenario Based Training
SDP Significance Determination Process

SG Steam Generator

Attachment

SI Safety Injection
SW Service Water
TDAFW Turbine Driven Auxiliary Feedwater
TDFWP Turbine Driven Main Feedwater Pump
TEDE Total Effective Dose Equivalent
TS Technical Specification
TSAS Technical Specification Action Statement
UFSAR Updated Final Safety Analysis Report
VHRA Very High Radiation Areas

WANO World Association of Nuclear Operators

WO Work Order