ML16314C026

From kanterella
Revision as of 03:56, 21 January 2019 by StriderTol (talk | contribs) (Created page by program invented by StriderTol)
Jump to navigation Jump to search
Comanche Peak Nuclear Power Plant - NRC Integrated Inspection Report 05000445/2016003 and 05000446/2016003
ML16314C026
Person / Time
Site: Comanche Peak  Luminant icon.png
Issue date: 11/08/2016
From: Groom J R
NRC/RGN-IV/DRP/RPB-A
To: Peters K
TEX Operations Company
JEREMY GROOM
References
IR 2016003
Download: ML16314C026 (29)


See also: IR 05000445/2016003

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION IV 1600 E. LAMAR BLVD.

ARLINGTON, TX

76011-4511 November 8, 2016 Mr. Ken Peters, Senior Vice President

and Chief Nuclear Officer

TEX Operations Company LLC

P.O. Box 1002

Glen Rose, TX 76043

SUBJECT: COMANCHE PEAK NUCLEAR POWER PLANT - NRC INTEGRATED INSPECTION REPORT 05000445/2016003

and 05000446/

2016003 Dear Mr. Peters: On September 30, 2016, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Comanche Peak Nuclear Power Plant, Units 1 and 2. O n September 29 , 2016, the NRC inspectors discussed the results of this inspection

with Mr. S. Sewell , Senior Director of Engineering and Regulatory Affairs, and other members of your staff. Inspectors documented the results of this inspection in the enclosed inspection report.

NRC inspectors documented two findings of very low safety significance (Green) in this report. All of these findings involved violations of NRC requirements.

If you contest the violations or significance of these NCVs, you should provide a response within

30 days of the date of this inspection report, with the basis for your denial, to the U.S.

Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555

-0001; and the NRC

resident inspector at the Comanche Peak Nuclear Power Plant, Units 1 and 2. If you disagree with

a cross-cutting aspect assignment

in this report, you should provide a response within 30

days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region IV; and the NRC

resident inspector at the Comanche Peak Nuclear Power Plant, Units 1 and 2. In accordance with Title 10 of the Code of Federal Regulations

(10 CFR) 2.390, "Public Inspections, Exemptions, Requests for Withholding,"

a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC

's Public Document Room or from the Publicly Available Records (PARS) component of the NRC's

K. Peters - 2 - Agencywide

Documents Access and Management System (ADAMS).

ADAMS is accessible from the NRC Web

site at http://www.nrc.gov/reading

-rm/adams.html

(the Public Electronic Reading Room).

Sincerely, /RA/ Jeremy R. Groom, Branch Chief Project Branch A

Division of Reactor Projects

Docket Nos.

50-445 and 50-446 License Nos. NPF-87 and NPF

-89 Enclosure: Inspection Report 05000445/2016003 and

05000446/2016003

w/ Attachment: Supplemental Information

cc w/ encl: Electronic Distribution

SUNSI Review

By: JRG ADAMS Yes No Non-Sensitive Sensitive Publicly Available

Non-Publicly Available

Keyword: NRC-002 OFFICE SRI:DRP/A RI:DRP/A SPE:DRP/A BC:EB1 BC:EB2 BC:OB BC:PSB2 NAME JJosey RKumana RAlexander

TFarnholtz

GWerner VGaddy HGepford SIGNATURE /RA/ /RA/ /RA/ /RA/ /RA/ /RA/ /RA/ DATE 10/21/16 10/24/16 10/19/16 10/19/16 10/25/16 10/20/16 10/20/16 OFFICE TL-IPAT BC:DRP/A NAME THipschman

JGroom SIGNATURE /RA/ /RA/ DATE 10/19/16 11/8/16

Letter to Ken Peters from Jeremy Groom dated November 8, 2016 SUBJECT: COMANCHE PEAK NUCLEAR POWER PLANT

-NRC INTEGRATED

INSPECTION REPORT 05000445/201

6 00 3 and 05000446/201

6 00 3 DISTRIBUTION

Regional Administrator (Kriss.Kennedy@nrc.gov)

Deputy Regional Administrator (Scott.Morris@nrc.gov) DRP Director (Troy.Pruett@nrc.gov)

DRP Deputy Director (Ryan.Lantz@nrc.gov) DRS Director (Anton.Vegel@nrc.gov)

DRS Deputy Director (Jeff.Clark@nrc.gov)

Senior Resident Inspector (Jeffrey.Josey@nrc.gov)

Resident Inspector (Rayomand.Kumana@nrc.gov)

Administrative Assistant (VACANT) Branch Chief, DRP/A (Jeremy.Groom@nrc.gov)

Senior Project Engineer, DRP/A (Ryan.Alexander@nrc.gov)

Project Engineer, DRP/A (Thomas.Sullivan@nrc.gov)

Project Engineer, DRP/A (Mathew.Kirk@nrc.gov)

Public Affairs Officer (Victor.Dricks@nrc.gov)

Project Manager (Margaret.Watford@nrc.gov) Team Leader, DRS/IPAT (Thomas.Hipschman@nrc.gov) RITS Coordinator (Marisa.Herrera@nrc.gov)

ACES (R4Enforcement.Resource@nrc.gov)

Regional Counsel (Karla.Fuller@nrc.gov) Congressional Affairs Officer (Jenny.Weil@nrc.gov)

RIV Congressional Affairs Officer (Angel.Moreno@nrc.gov)

RIV/ETA: OEDO (Jeremy.Bowen@nrc.gov) ROPreports

Electronic Distribution for Comanche Peak Nuclear Power Plant

A-1 Attachment

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV Docket: 05000445, 05000446

License: NPF-87, NPF-89 Report: 05000 445/20 16003 and 05000446/201600

3 Licensee: TEX Operations

Company, LLC

Facility: Comanche Peak Nuclear Power Plant, Units 1 and 2

Location: 6322 N. FM

-56, Glen Rose, Texas

Dates: July 1 through September 30, 2016 Inspectors:

J. Josey, Senior Resident Inspector

R. Kumana, Resident Inspector

W. Cullum, Reactor Inspector

Approved By: Jeremy R. Groom

Chief, Project Branch

A Division of Reactor Projects

A-2 SUMMARY IR 05000445/2016003 and 05000446/2016003

07/01/2016 - 09/3 0/2016; Comanche

Peak NPP, Units 1 and 2

Maintenance Effectiveness

, Problem Identification and Resolution

The inspection activities described in this report were performed between July 1, 2016, through September 30, 2016, by the resident inspectors at the Comanche Peak

Nuclear Power Plant

and an inspector from the NRC's Region IV office. Two finding s of very low safety significance (Green) are documented in this report. Both of these finding s involved a violation of NRC requirements. The significance of inspection findings is indicated by their color (Green, White,

Yellow, or Red), which is determined using Inspection Manual Chapter 0609, "Significance Determination Process." Their cross

-cutting aspects are determined using Inspection

Manual Chapter 0310, "Aspects within

the Cross-Cutting Areas." Violations of NRC requirements are dispositioned in accordance with the NRC Enforcement Policy. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in

NUREG-1649, "Reactor Oversight Process."

Cornerstone: Initiating Events

Green. The inspectors identified a non

-cited violation of 10 CFR 50.65(a)(4), "Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants," for

the licensee's failure to adequately manage the increase in risk associated with the potential for a loss of decay heat removal during refueling outages.

Specifically, the licensee implemented a risk management action that did not reduce the risk

, but instead called for placing a safety injection pump in service during periods where this action is prohibited by plant's technical specifications for low temperature over pressure protection. The inspectors determined this was an ineffective risk management action because the use of a safety injection pump during low pressure and temperature conditions would place the plant in an unanalyzed condition, resulting in an increase in risk. As an immediate corrective action, the licensee initiated Condition Report CR

-2015-009109 to evaluate appropriate risk management actions. This finding was entered into the licensee's corrective action program as Condition

Report CR-2015-009109.

The failure to manage the increase in ris

k associated with the potential for a loss of decay heat removal during refueling activities is a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it was associated with the procedure quality attribute of the Initiating Events Cornerstone and affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Using Inspection Manual Chapte

r 0609, Appendix K, "Maintenance Risk Assessment and Risk Management Significance Determination Process," dated May 19, 2005, Flowchart 1, "Assessment of Risk Deficit," the inspectors determined the need to calculate the risk deficit to determine the significance of this issue. A senior reactor analyst performed a bounding qualitative assessment and determined the incremental core damage probability deficit was less than 1E

-6 and the incremental large early release probability deficit was less than 1E

-7, based on the availability of additional equipment to mitigate the loss of decay heat removal. In

accordance with Flowchart 1 in Appendix K, because incremental core damage probability deficit was less than 1E

-6 and incremental large early release probability deficit was less than 1E-7, the finding screened as having very low safety significance (Green).

The finding has a human performance cross

-cutting aspect associated with bases for decisions, in that, the licensee failed to ensure that operations leadership adequately communicate potential

A-3 problems with the risk management action to start a safety injection pump when in a mode of applicability for low temperature over pressure protection [H.10]. (Section 4OA2)

Cornerstone: Mitigating Systems

Green. The inspectors identified a non

-cited violation of 10 CFR 50.65(a)(2), "Requirements for monitoring the effectiveness of maintenance at nuclear power plants." Specifically, the licensee failed to demonstrate that the performance of the Unit 2 auxiliary feedwater check valves was being effectively controlled through the performance of appropriate preventive maintenance. The licensee's failure to perform appropriate maintenance resulted in several failures of the check valves. The licensee entered this issue into corrective action program as CR-2016-008312. The licensee's failure to effectively monitor the performance of maintenance rule scoped

equipment in accordance with 10 CFR 50.65(a)(2) was a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it was associated with the equipment performance attribute of the Mitigating Systems Cornerstone

and affected the cornerstone objective to ensure availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the licensee failed to demonstrate that the performance of the Unit 2 auxiliary feedwater check valves was being effectively controlled through the performance of appropriate

preventive maintenance which resulted in failures of the valves. Using Inspection Manual Chapter (IMC) 0609, Appendix A, "The Significance Determination Process (SDP) for Findings At

-Power," dated June 19, 2012, inspectors determined that this finding was of very low safety significance (Green) because the finding (1) was not a deficiency affecting the design and qualification of a mitigating structure, system, or component, and did not result in a loss of operability or functionality, (2) did not represent a loss of system and/or function, (3) did not represent an actual loss of function of at least a single train for longer than its allowed outage time, or two separate safety systems out

-of-service for longer than their technical specification allowed outage time, and (4) did not represent an actual loss of function of one or more non

-technical specification trains of equipment designated as high safety-significant for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> in accordance with the licensee's maintenance rule program. A cross-cutting aspect was not assigned to this finding because the performance deficiency occurred in 1996, and therefore, is not indicative of current licensee performance. (Section 1R12)

Licensee-Identified Violations

None

A-4 PLANT STATUS

Unit 1 and Unit 2 began the inspection period at approximately 100 percent power and operated at that power level for the entire inspection period.

REPORT DETAILS

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1 R 01 Adverse Weather Protection (71111.01)

.1 Summer Readiness for Offsite and Alternate

AC Power Systems a. Inspection Scope

On July 20, 2016, the inspectors completed an inspection of the station's off

-site and alternate-ac power systems.

The inspectors inspected the material condition of these systems, including transformers and other switchyard equipment

to verify that plant features and procedures were appropriate for operation and continued availability of off

-site and alternate

-ac power systems. The inspectors reviewed outstanding work orders and open condition reports for these systems

. The inspectors walked down the switchyard to observe the material condition of equipment providing off-site power sources. The inspectors verified that the licensee's procedures included appropriate measures to monitor and maintain availability and reliability of the off

-site and alternate

-ac power systems.

These activities constitute

d one sample of summer

readiness

of off-site and alternate

-ac power systems , as defined in Inspection Procedure

71111.01. b. Findings No findings were identified.

1 R 04 Equipment Alignment (71111.04)

.1 Partial Walk

-Down a. Inspection Scope

The inspectors performed partial system walk

-downs of the following risk

-significant systems: August 4, 2016, Unit 2 , turbine driven and motor driven auxiliary feedwater pumps August 23, 2016, Unit 1, train A 125

V DC distribution system

September 20, 2016, Unit

s 1 and 2 , fire protection piping in the service water intake structure

A-5 The inspectors reviewed the

licensee's

procedures and system design information to determine the correct lineup for the systems. They visually verified that critical portions of the systems or trains were correctly aligned

for the existing plant configuration

. These activities constitute d three partial system walk

-down samples as defined i

n Inspection Procedure

71111.04. b. Findings No findings were identified

. 1 R 05 Fire Protection (71111.05)

.1 Quarterly Inspection

a. Inspection Scope

The inspectors evaluated the licensee's fire

protection program for operational status and material condition. The inspectors focused their inspection

on four plant areas important to safety

August 5, 2016, Fire area 2SC7, Unit 2 turbine driven auxiliary feedwater pump room September 19, 2016, Fire area SB2a, Unit 1 train A residual heat removal, safety injection, containment spray pumps rooms

September 19, 2016, Fire area SE16, Unit 1 Electrical

Equipment Room September 19, 2016, Fire area 2SE16, Unit 2 Electrical

Equipment Room For each area, the inspectors evaluated the fire plan against defined hazards

and defense-in-depth features in the licensee's fire protection program. The inspectors evaluated control of transient combustibles and ignition sources, fire detection and suppression systems, manual firefighting equipment and capability, passive fire protection features, and compensatory measures for degraded conditions.

These activities constitute

d four quarterl y inspection sample

s , as defined in Inspection Procedure 71111.05. b. Findings No findings were identified.

A-6 .2 Annual Inspection

a. Inspection Scope

On September 20, 2016, the inspectors completed their annual evaluation of the licensee's fire brigade performance. This evaluation included observation of two fire drills: March 22, 2016, Unit 1

, announced drill, contaminated waste fire drill, 832 foot corridor June 22, 2016, Unit 2

, announced drill, 858 foot elevation valve gallery

During these drills the inspectors evaluated the capability of the fire brigade members, the leadership ability of the brigade leader, the brigade's use of turnout gear and fire

-fighting equipment, and the effectiveness of the fire brigade's team operation. The inspectors also reviewed whether the licensee's fire brigade met NRC requirements for training, dedicated size and membership, and equipment.

These activities constitute

d one annual inspection sample , as defined in Inspection Procedure 71111.05. b. Findings No findings were identified.

1 R 06 Flood Protection Measures (71111.06)

a. Inspection Scope

On September 23, 2016, the inspectors completed an inspection of the station's ability to mitigate flooding due to internal causes. After reviewing the licensee's flooding analysis, the inspectors selected one plant area containing risk

-significant structures, systems, and components that were susceptible to flooding:

Unit s 1 and 2, service water intake structure

The inspectors reviewed plant design features and licensee procedures for coping with

internal flooding. The inspectors walked down the selected areas to inspect the design features, including the material condition of seals, drains, and flood barriers. The

inspectors evaluated whether operator actions credited for flood mitigation could be successfully accomplished.

These activities constitute

d completion of

one flood protection measures sample

as defined in Inspection Procedure

71111.06. b. Findings No findings were identified.

A-7 1 R 11 Licensed Operator Requalification Program and Licensed Operator Performance (71111.11)

.1 Review of Licensed Operator Requalification

a. Inspection Scope

On September 27, 2016, the inspectors observed

a portion of an annual requalification test for licensed operators. The inspectors assessed the performance of the operators

and the evaluators' critique of their performance.

These activities constitute

d completion of one quarterly licensed

operator requalification program sample , as defined in Inspection Procedure

71111.11. b. Findings No findings were identified.

.2 Review of Licensed Operator Performance

a. Inspection Scope

Inspectors observed the performance of on

-shift licensed operators in the plant's main control room. At the time of the observations, the plant was in a period of heightened activity or risk due to testing being performed on reactor protection and response

to unusual plant conditions.

The inspectors observed the operators' performance of the following activities:

July 13, 2016, Unit 2, Observation during slave relay testing

August 8, 2016, Unit 2, Observation of operators response to heater drain pump

seal water low pressure alarm

September 26, 2016, Unit 1, Observation of reactor trip breaker testing

In addition, the inspectors assessed the operators' adherence to plant procedures, including conduct of operations procedure and other operations department policies.

These activities constitute

d completion of

one quarterly licensed

operator performance sample , a s defined in Inspection Procedure

71111.11. b. Findings No findings were identified.

1 R 12 Maintenance Effectiveness (71111.12)

a. Inspection Scope The inspectors reviewed

t wo instances of degraded performance or condition of safety

-related structures, systems, and components

(SSCs):

A-8 August 20, 2016, Unit 2, main feedwater system split flow bypass check valves

September 23, 2016, Unit 1, pressurizer heater group C blown fuse

The inspectors reviewed the extent of condition of possible common cause SSC failures and evaluated the adequacy of the licensee's corrective actions. The inspectors reviewed the licensee's work practices to evaluate whether these may have played a role in the degradation of the SSCs. The inspectors assessed the licensee's characterization of the degradation

in accordance with 10 CFR 50.65 (the Maintenance Rule), and verified that the licensee was appropriately tracking degraded performance and conditions in accordance with the Maintenance Rule.

These activities constitute

d completion of

t wo maintenance effectiveness samples , a s defined in Inspection Procedure

71111.12. b. Findings Introduction. The inspectors identified a Green

, non-cited violation of 10 CFR 50.65(a)(2), "Requirements for monitoring the effectiveness of maintenance at nuclear power plants."

Specifically, the licensee failed to demonstrate that the performance of the Unit 2 auxiliary feedwater check valves was being effectively controlled through the

performance of appropriate preventive maintenance.

Description. On November 11, 2015, the licensee conducted in

-service testing on feedwater check valve 2FW

-0191, one of four steam generator split flow bypass check valves. During the test, check valve 2FW

-0191 failed to meet the site's acceptance criteria indicating the valve failed to seat. The licensee stopped the test and initiated Condition Report CR

-2015-10961 to document the test failure.

Subsequently, the system engineer performed a maintenance rule functional failure review of this issue. This review determined that the failure of valve 2FW

-0191 to seat was not a maintenance rule functional failure and the function would remain in (a)(2)

status. Inspectors questioned this assessment because one of the scoped functions of this feedwater check valve is to shut to prevent bypassing flow from the steam

generators. During discussions with the licensee, the inspectors determined that system engineer was only evaluating the split flow check valves performance against the main feedwater system's criteria to provide feedwater to the steam generator, and not against the criteria related to the valve's ability to shut to prevent bypassing flow from the steam generators. Inspectors also determined that the licensee was not performing preventative maintenance on the check valves to ensure their ability to close and seat properly. The inspectors subsequently reviewed the last test data for all four of the steam generator split flow bypass check valves.

In this review the inspectors noted that in 2011 valve 2FW

-0192 had failed to meet the established acceptance criteria, yet the failure was not noted as a functional failure. Additionally, in 2012 , valves 2FW-0191, 2FW-0192, and 2FW-0193 all failed to meet the established acceptance criteria, and again the failures were not noted as functional failures.

The inspectors noted that 10 CFR 50.65(a)(2) requires, in part, that monitoring as specified in 10 CFR 50.65(a)(1) is not required where it has been demonstrated that the

A-9 performance of a system is being effectively controlled through the performance of appropriate preventive maintenance, such that the system remains capable of performing its intended function. Based on their review, the inspectors determined that the licensee failed to demonstrate that the performance of the Unit 2 feedwater check

valves was being effectively controlled. Specifically, the licensee was not performing preventative maintenance on the check valves, resulting in the valves failing to close on

multiple occasions during testing.

The inspectors informed the licensee of the concerns and the licensee initiated condition report CR-2016-008312 to capture this issue in the station's

corrective action program. The licensee recognized that they were not correctly monitoring the function of these check valves. Specifically, the

licensee determined that monitoring the check valves only as part of the main feedwater system was not adequate since the system's performance criteria is to provide feedwater to the steam generators

, and the check valves function is to close to prevent bypass flow. The licensee subsequently performed a review to determine if other safety

-related check valves were also not being monitored correctly. Based on this review the licensee determined that there were 841 safety

-related check valves (of which 230 were classified as run to failure) that were not being monitored against their scoped criteria. To correct this issue, the licensee created a new monitoring function for safety related check valves which monitors the close function, and moved the equipment to 10

CFR 50.65(a)(1) monitoring requirements because they determined that they were not able to demonstrate that the performance of the check

valves was being effectively controlled.

Analysis. The licensee's failure to effectively monitor the performance of maintenance rule scoped equipment in accordance with 10 CFR 50.65(a)(2) was a performance

deficiency.

The performance deficiency was more than minor, and therefore a finding, because it was associated with the equipment performance attribute of the Mitigating

Systems Cornerstone and affected the cornerstone objective to ensure availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the licensee failed to demonstrate that the

performance of the Unit 2 auxiliary feedwater

check valves was being effectively controlled through the performance of appropriate preventive maintenance which resulted in failures of the valves. Using Inspection Manual Chapter (IMC) 0609, Appendix A, "The Significance Determination Process (SDP) for Findings At

-Power," dated June 19, 2012, inspectors determined that this finding was of very low safety

significance (Green) because the finding (1) was not a deficiency affecting the design and qualification of a mitigating structure, system, or component, and did not result in a loss of operability or functionality, (2) did not represent a loss of system and/or function, (3) did not represent an actual loss of function of at least a single train for longer than its allowed outage time, or two separate safety systems out

-of-service for longer than their technical specification allowed outage time, and (4) did not represent an actual loss of

function of one or more non

-technical specification trains of equipment designated as high safety

-significant for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> in accordance with the licensee's maintenance rule program.

A cross-cutting aspect was not assigned to this finding because the performance deficiency occurred in 1996

when the steam generator split flow bypass check valve was initially scoped under the Maintenance Rule, and therefore, is not indicative of current licensee performance.

Enforcement. Title 10 CFR 50.65(a)(1) requires, in part, that holders of an operating license shall monitor the performance of systems and components against licensee

A-10 established goals, in a manner sufficient to provide reasonable assurance that such structures, systems, and components are capable of fulfilling their intended safety functions. 10 CFR 50.65(a)(2) states, in part, that monitoring as specified in 10 CFR 50.65(a)(1) is not required where it has been demonstrated that the performance of a

system is being effectively controlled through the performance of appropriate preventive maintenance, such that the system remains capable of performing its

intended function. Contrary to the above, from initial maintenance rule scoping in 1996 to September 2016, the licensee did not monitor the performance of the Unit 2 auxiliary feedwater system check valves against licensee

-established goals in a manner sufficient to provide reasonable assurance that the check valves were capable of fulfilling their intended

safety functions, and the licensee did not demonstrate that the performance of check

valves was being effectively controlled through the performance of appropriate preventive maintenance, such that the system remained capable of performing its

intended function. In response to this issue the licensee created a new monitoring function for safety related check valves, and moved the equipment to 10 CFR

50.65(a)(1) monitoring requirements pending further review. Since this violation was of very low safety significance (Green) and has been entered into the corrective action program as Condition Report CR-2016-008312, this violation

is being treated as a non

-cited violation consistent with Section 2.3.2 of the NRC Enforcement Policy. (NCV 05000446/201600 3-0 1, Failure to Adequately Monitor Feedwater System Check Valve Performance

) 1 R 13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a. Inspection Scope

On July 7, 2016, the inspectors reviewed a risk assessment and the risk management actions taken by the licensee in response to elevated risk associated with

performing an oil sample on spent fuel pool pump X

-01. The inspectors verified that this risk assessment was performed timely and in accordance with the requirements of 10 CFR 50.65 (the Maintenance Rule) and plant

procedures. The inspectors reviewed the accuracy and completeness of the licensee's risk assessment and verified that the licensee implemented appropriate risk management actions based on the result of the assessment.

The inspectors also observed portions of three emergent work activities that had the potential to affect the functional capability of mitigating systems:

August 18, 2016, Unit 2, Steam generator blowdown isolation valve 2

-HV-2399 elastomer replacement

September 1, 2016, Unit s 1 and 2, unanalyzed condition associated with the turbine driven auxiliary feedwater pumps

September 16, 2016, Unit 2, loop A safety chiller emergent maintenance

The inspectors verified that the licensee appropriately developed and followed a work plan for these activities. The inspectors verified that the licensee took precautions to minimize the impact of the work activities on unaffected SSCs.

A-11 These activities constitute

d completion of four maintenance risk assessments and emergent work control inspection samples , as defined in Inspection Procedure

71111.13. b. Findings No findings were identified.

1 R 15 Operability Determinations

and Functionality Assessments

(71111.15)

a. Inspection Scope

The inspectors reviewed seven operability determinations that the licensee performed for degraded or nonconforming SSCs:

March 28, 2016, CR

-2016-003089, operability determination for control room air conditioner X

-01 partial refrigerant charge

July 12, 2016, CR

-2016-006613, operability determination for

diesel generator

2-01 86-2 lockout relay actuation August 22, 2016, CR-2016-007251, operability determination

for turbine driven

auxiliary feedwater pump 1

-01 indicating light socket/bulb melted

August 24, 2016, CR-2016-007653, operability determination for motor driven auxiliary feedwater pump room heat up analyses

August 31, 2016

, CR-2016-007840, operability determination for safety injection pump 2-01 oil leak

September 8, 2016, CR-2016-008000, operability determination for diesel generator

2-0 1 failed KVAR meter

September 21, 2016, CR

-2016-007880, operability determination for auxiliary feedwater pumps following identification of an unanalyzed condition

The inspectors reviewed the timeliness and technical adequacy of the licensee's evaluations. Where the licensee determined the degraded SSC to be operabl

e the inspectors verified that the licensee's compensatory measures were appropriate to provide reasonable assurance of operability. The inspectors verified that the licensee had considered the effect of other degraded conditions on the operability of the degraded SSC

.

These activities constitut

e d completion of seven operability and functionality review

samples , as defined in Inspection Procedure

71111.15. b. Findings No findings were identified.

A-12 1 R 18 Plant Modifications (71111.18)

.1 Temporary Modifications

a. Inspection Scope

On September 15, 2016, the inspectors review

ed a temporary plant modification

to remove sentinel valves from the turbine driven auxiliary feedwater pumps on Unit 1

and 2. The inspectors verified that the licensee had installed these temporary modifications in accordance with technically adequate design documents. The inspectors verified that these modifications did not adversely impact the operability or availability of affected SSCs. The inspectors reviewed design documentation and plant procedures affected by

the modifications to verify the licensee maintained configuration control.

These activities constitute

d completion of

one sample of temporary modifications, as defined in Inspection Procedure

71111.18. b. Findings No findings were identified.

1 R 19 Post-Maintenance

Testing (71111.19)

a. Inspection Sco

pe The inspectors reviewed four post-maintenance testing activities that affected risk

-significant SSCs:

April 5, 2016, Unit 1, offsite power supply breaker 1EA2-1 post maintenance test

May 25, 2016, Unit 1, service water

pump 1-01 replacement

August 23, 2016, Unit 2, Steam generator 2

-03 blowdown isolation valve

2-HV-2399 testing following elastomer replacement

September 15, 2016, Unit 1 and Unit 2, turbine driven auxiliary feedwater pumps following temporary modification

The inspectors reviewed licensing and design

-basis documents for the SSCs and

the maintenance

and post-maintenance test procedures.

The inspectors observed the performance of the post

-maintenance tests to verify that the licensee performed the tests in accordance with approved procedures, satisfied the established acceptance criteria, and restored the operability of the affected SSCs

. These activities constitute

d completion of four post-maintenance

testing inspection samples , a s defined in Inspection Procedure

71111.19.

A-13 b. Findings No findings were identified.

1 R 22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors observed four risk-significant surveillance tests and reviewed test results to verify that these tests adequately demonstrated that the SSCs were capable of performing their safety functions:

Other surveillance tests:

May 26, 2016, Unit 1, stroke test of power operated relief valve

1-PCV-456 August 5, 2016, Unit 2, start and flow test of the turbine driven auxiliary feedwater pump

August 23, 2016, Unit 1, stroke test of

containment sump pump discharge line outside-containme nt isolation valve 1

-HV-5157 September 8, 2016, Unit 2, start test of diesel generator 2

-01

The inspectors verified that these test

s met technical specification requirements, that the licensee performed the tests in accordance with their procedures, and that the results of the test satisfied appropriate acceptance criteria. The inspectors verified that the licensee restored the operability of the affected SSCs following testing.

These activities constitute

d completion of four surveillance testing inspection samples , as defined in Inspection Procedure

71111.22. b. Findings No findings were identified.

Cornerstone: Emergency Preparedness

1 EP 6 Drill Evaluation (71114.06)

.1 Emergency Preparedness Drill Observation

a. Inspection Scope

The inspectors observed an emergency preparedness drill on September 28, 2016, to verify the adequacy and capability of the licensee's assessment of drill performance.

The inspectors reviewed the drill scenario, observed the drill from the simulator and emergency operations facility, and attended the post

-drill critique. The inspectors verified that the licensee's emergency classifications, off

-site notifications, and protective action recommendations were appropriate and timely. The inspectors verified that any

A-14 emergency preparedness weaknesses were appropriately identified by the licensee in the post-drill critique and entered into the corrective action program for resolution.

These activities constitute

d completion of

one emergency preparedness drill observation sample, as defined in Inspection Procedure

71114.06. b. Findings No findings were identified.

4. OTHER ACTIVITIES

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Security 4OA 1 Performance Indicator Verification (71151)

.1 Mitigating Systems Performance Index:

Emergency AC Power System

s (MS06) a. Inspection Scope

The inspectors reviewed the licensee's mitigating system performance index data for the

period of July 1, 2015

through June 30, 2016

to verify the accuracy and completeness of the reported data. The inspectors used definitions and guidance contained in

Nuclear Energy Institute Document

99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7, to determine the accuracy of the reported

data. These activities constituted verification of the mitigating system performance index for emergency ac power systems for Units 1 and 2, as defined in Inspection Procedure 71151. b. Findings No findings were identified.

.2 Mitigating Systems Performance Index: High Pressure Injection Systems (MS07)

a. Inspection Scope

The inspectors reviewed the licensee's mitigating system performance index data for the

period of July 1, 2015 through June 30, 2016 to verify the accuracy and completeness of the reported data. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document

99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7, to determine the accuracy of the reported data.

These activities constituted verification of the mitigating system performance index for high pressure injection systems for Units 1 and 2, as defined in Inspection Procedure 71151.

A-15 b. Findings No findings were identified.

.3 Mitigating Systems Performance Index

Heat Removal System

s (MS08) a. Inspection Scope

The inspectors reviewed the licensee's mitigating system performance index data for the period of July 1, 2015 through June 30, 2016 to verify the accuracy and completeness of the reported data. The inspectors used definitions and

guidance contained in Nuclear Energy Institute Document

99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7, to determine the accuracy of the reported data.

These activities constituted verification of the mitigating system performance index for heat removal systems for Units 1 and 2, as defined in Inspection Procedure

71151. b. Findings No findings were identified.

4OA 2 Problem Identification and Resolution

(71152) .1 Routine Review

a. Inspection Scope

Throughout the inspection period, the inspectors performed daily reviews of

items entered into the licensee's corrective action program

and periodically attended the licensee's condition report screening meetings. The inspectors verified that licensee personnel were identifying problems at an appropriate threshold and entering these problems into the corrective action program for resolution. The inspectors verified that the licensee developed and implemented corrective actions commensurate with the significance of the problems identified.

The inspectors also reviewed the licensee's problem identification and resolution activities during the performance of the other inspection activities documented in this report.

b. Findings No findings were identified.

.2 Annual Follow

-up of Selected Issues

a. Inspection Scope

The inspectors selected

two issue s for an in-depth follow

-up: During refueling outage 2RF15, October 2015, and refueling outage 1RF18,

May 2016, the licensee credited defense in depth contingency plans, risk assessments with specified risk management actions, for time periods when the reactor coolant system would be in a loops not filled condition or when shutdown

A-16 cooling would be in a reduced availability condition due to the increase in risk for the activities

. The inspectors assessed the licensee's risk assessments and the specified risk management actions. The inspectors identified that the licensee failed to

appropriately manage the risk associated with the activities.

On May 18, 2016, after completion of preventative maintenance on the lube oil cooler for coolant charging pump 1

-01, a service water leak was discovered coming from the cooler head. Upon disassembly, the licensee discovered

significant pitting on the head

for the heat exchanger. The licensee initiated Condition Report 2016

-004868 to evaluate the issue, though an operability evaluation was not performed at the time because the unit was not in a mode of applicability for the charging pump. The licensee determined that this condition had been previously identified in Condition Report CR

-2014-001804, and parts were on order to replace the pitted head. The licensee's corrective action was to apply Loctite #2, a sealant material, to stop the leak, noting that this had previously been evaluated as acceptable in Condition Report CR

-2006-001208.

Upon further review inspectors determined that the evaluation performed in CR

-2006-001208 was a one

-time evaluation for use of Loctite #2, and did not establish a basis for the current use. Therefore, an operability evaluation was required for the subsequent use of Loctite. The licensee initiated Condition Reports CR

-2016-004936 and CR

-2016-006674 to address this issue, and document ed a current operability evaluation for use of the Loctite.

Inspectors determined that this issue was a minor violation of Title 10 CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," which requires, in part, that activities affecting quality shall be accomplished in accordance with documented instructions, procedures, or drawings, of a type

appropriate to the circumstances. Station Procedure STI

-442.01, "Operability Determination and Functionality Assessment Program," is an Appendix B quality related procedure

that is appropriate to the circumstances for evaluating the operability of safety

-related components. Station Procedure STI

-442.01 step 6.1, requires, in part, that when a potential degraded or nonconforming condition is identified, the shift manager should ensure the operability determination process is initiated to determine the operability of the structure, system or component.

The inspectors assessed the licensee's problem identification threshold, cause analyses, extent of condition reviews and compensatory actions. The inspectors verified that the licensee appropriately prioritized the planned corrective actions

and that these actions were adequate to correct the condition.

These activities constitute

d completion of two annual follow

-up sample a s defined i n Inspection Procedure

71152. b. Findings Introduction. The inspectors identified a Green non

-cited violation of

10 CFR 50.65(a)(4), "Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants," for the licensee's failure to adequately manage the increase in

A-17 risk associated with the potential for a loss of decay heat removal during refueling outages. Description. During refueling outage 2RF15, October 2015, when the licensee was setting up for vacuum fill of the reactor coolant system

, inspectors reviewed the station

's defense in depth contingency plan 2RF15

-01. The inspectors determined that this contingency plan was a risk assessment with specified risk management actions for periods when the reactor coolant system would be in a

"loops not filled condition

" or periods of reduced

availability of the shutdown cooling system. Inspectors noted that the contingency plan for these periods

of increased risk directed that if residual heat removal (shutdown cooling) is lost, operators should establish alternate cooling flow path using Station Procedure ABN

-104, "Residual Heat Removal System Malfunction," Revision 9, section 8.

Inspectors reviewed ABN

-104, section 8 and noted that it directed operators to start a safety injection pump

in response to a loss of shutdown cooling. Inspectors identified

a concern that

the action to start a safety injection pump would occur while in the mode of applicability for technical specification 3.4.12, "Low Temperature Overpressure Protection System

." Technical specification 3.4.12 requires the safety injection pumps be made incapable of injecting due to concerns of

over pressurizing the reactor coolant system in modes 4, 5, and 6 (the latter only when the reactor vessel head is installed). The licensee initiated Condition Report CR

-2015-009109 to capture th

e inspector's concern in the station

's corrective action program. Subsequently, during refueling outage 1RF18, May 2016, inspectors noted that the licensee again credited a defense in depth contingency plan (1RF18

-01) which again would have operators start a safety injection pump when technical specification 3.4.

12 was in effect. During subsequent reviews, the inspectors determined that the licensee did not have an evaluation for starting a safety injection pump when low temperature overpressure protection was in effect.

Inspectors determined that the specified risk management action to start a safety injection pump would restore flow to the core to mitigate the loss of shutdown cooling. However, the inspectors also determined that the plant is not analyzed for using a safety injection pump during periods when the reactor coolant system is at low temperatures requiring low temperature overpressure protection. The proposed use of safety injection

pumps as described in ABN

-104, section 8, without analyses for sufficient relief capability, created the potential for vessel overpressurization and a challenge to the reactor coolant system barrier. Any challenge to the reactor coolant system barrier

would serve to increase risk. The inspectors also noted that the licensee had several options to mitigate a potential loss of shutdown cooling that are analyzed during period where low temperature overpressure protection is required. Specifically, the inspectors

identified that the licensee could start centrifugal charging pumps to restore core flow following a loss of shutdown cooling. These pumps have slightly less capacity than the safety inspection pumps which would be bounded by the relief capability required in

technical specification 3.4.12.

Inspectors informed the licensee of the

additional

concerns and the licensee added them to Condition Report CR

-2015-009109. Inspectors determined that the licensee had not started a safety injection pump when technical specification 3.4.12 was in effect

during

A-18 1RF19 or 2RF18. As corrective actions, the license

e amend ed Condition Report

CR-2015-009109 to evaluate appropriate risk management actions.

Analyses. The failure to manage the increase in risk associated with the potential for a loss of decay heat removal during refueling activities is a performance deficiency. The performance deficiency was more than minor, and therefore a finding, because it was associated with the procedure quality attribute of the Initiating Events Cornerstone and affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power

operations. Using Inspection Manual Chapter 0609, Appendix K, "Maintenance Risk Assessment and Risk Management Significance Determination Process," dated May 19, 2005, Flowchart 1, "Assessment of Risk Deficit," and determined the need to calculate the risk deficit to determine the significance of this issue. A senior reactor analyst performed a bounding qualitative assessment, using insights from Inspection Manua

l Chapter 0609, Appendix G, "Shutdown Operations Significance Determination Process,"

and determined the incremental core damage probability deficit was less than 1E

-6 and the incremental large early release probability deficit was less than 1E

-7. The influential assumptions used by the senior reactor analyst included the low exposure time that the

plant is in LTOP conditions, the initiating event frequency associated with a loss of decay heat removal, available operator mitigation

actions that would prevent the use of safety injection pumps

, and the availability of additional equipment to mitigate the loss of decay heat removal.

In accordance with Flowchart 1

in Appendix K, because incremental core damage probability deficit was less than 1E

-6 and incremental large early release probability deficit was less than 1E

-7, the finding screened as having very low safety significance (Green). The finding has a human performance cross

-cutting aspect associated with bases for decisions, in that, the licensee failed

to ensure that operations leadership adequately communicate potential problems with the risk management action to start a safety injection pump when in a mode of applicability for low temperature over pressure protection [H.10]. Enforcement. Title 10 CFR 50.65(a)(4) requires, in part, that licensees shall asses s and manage the increase in risk that may result from proposed maintenance activities. Defense in depth contingency plan

s 2RF15-01 and 1RF18

-01 implement pre

-planned risk assessments and specified risk management actions for times during refueling outages when the reactor coolant system is depressurized and level is lowered. Contrary to the above, from October 3, 2015, through May 31, 2016, the licensee failed to manage the increase in risk from proposed maintenance activities. Specifically, the licensee implemented a risk management action that did not reduce the risk, instead it called for placing the plant in an unanalyzed condition which

could elevate risk. As an immediate corrective action the licensee initiated Condition Report CR

-2015-009109 to evaluate appropriate risk management actions. Since this violation was of very low

safety significance (Green) and has been entered into the corrective action program as Condition Report

CR-2015-009109, this violation is being treated as a non

-cited violation consistent with Section 2.3.2 of the NRC Enforcement Policy. (NCV 05000445/201600

3-0 2; 05000446/201600

3-0 2, Failure to Manage Risk

During Refueling Outages

)

A-19 4OA 5 Other Activities

a. Inspection Scope The inspectors evaluated the impact of financial conditions on continued safe performance at Comanche Peak. I

n that t he licensee's pa r ent c o m pan y , E n e r g y F u t u r e H o l d i n g s , w as under bank

r up t cy p r o t e c t i on/r e o r g an i z a t i on du r i ng t he inspec t i on p e r i o d , NR C R e g io n IV condu c t ed spec ial r e v i e w s of p roce sses a t C o manche P e a k. T he inspec t o r s e v a l ua t ed se v e ral aspec t s o f t he licensee's ope r a ti ons t o d e t e r m i ne w he t her t he f i nanc ial cond i t i on o f t he s t a t i on i m pac t ed p lant s a f e t y. T he f a c t o r s r e v i e w e d i nc luded: (1) i m pa c t on s t a f f i ng, (2) co r r ec t i v e m a i n tenance ba c k l og, (3) chan ges t o t he p l anned m a i n t en ance schedu l e, (4) c o rr e c ti v e ac t i on p r o g r a m i m p l e m en t a t i on, and (5) r educ t i on i n o u t a g e scop e , i nc l ud i ng r i s k-s i g n i f icant m od i f i ca t i on s. I n pa r t i cu l a r , t he inspec t o r s v e r i f i ed t h a t licensee p e rsonnel con

t inued t o i den t i f y p r o b l e m s a t an app r o p r i a t e t h resho l d and e n t er these p r ob l e m s i n t o t he c o rr e c ti v e ac t i on p r o g r a m for r e so l u t i on. T he inspec t o r s a lso v e r i f i ed that t he licensee con t i nued t o de v e l op and i m p l e m e n t c o rr e c t i v e ac t ions co mm e n su r a t e w i t h t he s i g n i f icance o f t he p r ob l e m s i de n t i f ied. T he spec ial r e v i ew of p r ocesses a t C o manche P e ak i nc l uded con t i nuous r e v i e ws by t he R es ident Inspe c t o rs, as w e ll as t he spec i a li st-l ed base li ne inspec t i ons co m p l e t ed du r i n g t he i n s pec t i on pe r i od w h ich a r e doc u m en t ed p r e v i o u s l y i n t h i s r ep o r t. b. Findings No findings were identified.

4OA 6 Meetings, Including Exit

Exit Meeting Summary

On July 7, 2016, the resident inspectors presented the inspection results to Mr. S. Sewell , Senior Director of Engineering and Regulatory Affairs, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.

A-20 SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

G. Struble, Manager, Operations/Simulator Training

J. Alldredge, Technician, Radiation Protection

T. Curtis, Lead Environmental Technician

S. Darter, Coordinator, Radiation Protection

S. Dixon, Consulting Licensing Analyst/Regulatory Affairs

T. Emery, Technician , Radiological Environmental Monitoring Program

T. Hope, Manager, Regulatory Affairs

B. Knapp, Acting Manager, Radiation Protection

M. Macho, Supervi

sor, Radiation Protection

S. Peterson, Senior Calibration Laboratory Technician, Radiation Protection

K. Powell, Supervisor, Radiation Protection

M. Syed, Engineer, Systems Engineer

M. Watkins, Lead Technician, Instruments and Controls Maintenance

J. Barnette, Consultant, Licensing Technologist

S. Bartholomew, Analyst , Emergency Preparedness

G. Bryan, Operations Specialist, Emergency Preparedness

K. Faver, Planner , Emergency Preparedness

R. Fishencord, Planner, Emergency Preparedness

J. Hull, Manager, Emergency Preparedness

R. Marquez, Planner, Emergency Preparedness

S. Sewell, Senior Director of Engineering and Regulatory Affairs

D. Volkening, Manager, Nuclear Oversight

T. McCool, Site Vice President

B. Knowles, Radiation Protection Staff

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000446/201600 3-0 1 NCV Failure to Adequately Monitor Feedwater System Check Valve Performance

(Section 1R12)

05000445/201600

3-0 2;05000446/201600

3-0 2 NCV Failure to Manage Risk

During Refueling Outages

(Section 4OA2)

A-21 LIST OF DOCUMENTS REVIEWED

Section 1R01: Adverse Weather Protection

Procedures

Number Title Revision STA-629 Switchyard Control and Transmission Grid Interface

7 Section 1R04: Equipment Alignment

Condition Reports CR-2016-007245 Drawings Number Title Revision E1-0020 125V DC One Line Diagram

CP-20 E1-0021 Common Auxiliary Control Fuel and Turbine Buildings Normal 480VC MCCs One Line Diagram

CP-22 Procedures

Number Title Revision SOP-904 Fire Protection Main Water Supply and Fire Pumps System

16 OPT-215 Class 1E Electrical Systems Operability

15 Section 1R05: Fire Protection

Condition Reports

CR-2016-002654 Drawings Number Title Revision E1-2020 Safeguard Building Fire Detection Plan EL 773'

-0", 790'-6" and 800'-6" CP-2 Procedures

Number Title Revision SAF-104 Inspection of Respiratory Protection Equipment (Maintenance and Repair)

11

A-22 Procedures

Number Title Revision ABN-901 Fire Protection System Alarms or Malfunctions

2 FPI-103A Fire Preplan Instruction Manual, Unit 1 Safeguards Building Elevation 810'

-6", Rad. Pen. Area & Elec. Equip. Rm

4 Miscellaneous Documents

Number Title Revision -- Fire Protection Report

30 Work Orders

4789803 Section 1R06: Flood Protection Measures

Calculations

Number Title Revision SI-CA-0000-693 Miscellaneous Building

- Flooding Analysis

1 Section 1R11: Licensed Operator Requalification Program and Licensed Operator Performance

Procedures

Number Title Revision EOP-3.0A Steam Generator Tube Rupture

9 Section 1R13: Maintenance Risk Assessments and Emergent Work Control

Condition Reports

CR-2016-007272 CR-2016-000493 CR-2016-007720 CR-2016-007428 CR-2016-007690 Procedures

Number Title Revision DID XPWR-SFP-01 SFP Cooling During Non

-Refueling Outage Conditions

- STI-600.01 Protecting Plant Equipment and Sensitive Equipment Controls

1 MSM-GO-0213 Sway Strut Maintenance

1

A-23 Work Orders

5320735 5210636 Section 1R15: Operability Determinations and Functionality Assessments

Calculations

Number Title Revision 1-EB-302-4 As Built HVAC Calculation

- Auxiliary Feedwater Pump Room Unit 1 5 Condition Reports

CR-2016-003089 CR-2016-007251 CR-2016-007653 CR-2016-007840 Work Orders

5010266 Section 1R18: Plant Modifications

Miscellaneous Documents

Number Title Revision FDA-2016-000123-01-00 Create Temp Mod FDA to Remove the Sentinel Valves on the Casing of the TDAFW Pump Turbines

00 Work Orders

5330786 5330788 Section 1R19: Post

-Maintenance Testing

Condition Reports CR-2016-000493 CR-2016-007559 TR-2016-004759 CR-2016-005744 CR-2016-005216 CR-2016-003163 Drawings Number Title Revision E1-0031-07 6.9 kV Switchgear Bus 1EA2 Breaker 1EA2

-2 Schematic Diagram CP-13

A-24 Procedures

Number Title Revision MSM-G0-0213 Sway Strut Maintenance

1 MSM-G0-4004 Baker On-line Motor Testing

5 MSM-C0-7310 Service Water Pump Maintenance

5 SOP-603A 6900 V Switchgear

16 MSE-G0-0020 Relay Calibration

5 Work Orders

5210636 5330786 4297555 5008028 4947477 4986918 5008083 5136434 4913385 Section 1R22: Surveillance Testing

Condition Reports

CR-2016-007588 Drawings Number Title Revision M2-0206 Flow Diagram Auxiliary Feedwater System

CP-15 Procedures

Number Title Revision OPT-206B AFW System

22 OPT-503A Cntmt Isol Valves ASME Testing

15 Work Orders

5270846

Section 1EP6: Drill Evaluation

Procedures

Number Title Revision EPP-121 Re-Entry, Recovery and Closeout

10 EPP-116 Emergency Repair & Damage Control and Immediate Entries

9

A-25 Procedures

Number Title Revision EPP-109 Duties and Responsibilities of the Emergency Coordinator / Recovery Manager

15 ABN-907 Acts of Nature

15 Section 4OA2: Problem Identification and Resolution

Condition Reports

CR-2006-001208 CR-2014-001804 CR-2016-004868 CR-2016-004936