ML17223A524

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Monthly Operating Repts for Jan 1990 for St Lucie Units 1 & 2.W/900215 Ltr
ML17223A524
Person / Time
Site: Saint Lucie  NextEra Energy icon.png
Issue date: 01/31/1990
From: BONETT D M, SAGER D A
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
L-90-53, NUDOCS 9002260449
Download: ML17223A524 (16)


Text

DOCKETN0500033505000389gcCp~RATZDDlBUTIONDEMONSTR0.'iSYSTEMIREGULATOR1 NFORMATION DISTRIBUTION S2EM(RIDS)ACCESSION NBR:9002260449 DOC.DATE:

90/01/31NOTARIZED:

NOFACIL:50-335 St.LuciePlant,Unit3floridaPower6LightCo.50-389St.Lucie,Plant,Unit2,FloridaPower6LightCo.AUTH.NAMEAUTHORAFFILIATION BONETT,D.M.

FloridaPoweraLightCo.SAGER,D.A.

FloridaPoweraLightCo.RECIP.NAME RECIPIENT AFFILIATION

SUBJECT:

Monthlyoperating reptsforJan1990forStLucieUnits162.W/900215 ltr.DISTRIBUTION CODE:IE24DCOPIESRECEIVED:LTR gENCLgSIZE:(0TITLE:MonthlyOperating Report(perTechSpecs)NOTES:RECIPIENT IDCODE/NAME PD2-2LANORRISPJINTERNAL:

ACRSAEOD/DSP/TPAB NRR/DLPQ/LPEB10 EPPRPB11,REFILE01EXTERNAL:

EG&GSIMPSONPF NRCPDRCOPIESLTTRENCL33111010111111111111RECIPIENT IDCODE/NAME PD2-2PDAEOD/DOAIRMTECHADVNRR/DOEA/OEAB11 NUDOCS-ABSTRACT RGN2LPDRNSICCOPIESLTTRENCL1111221111111111NCTEIOALL"RIDS"RECIPZEÃIS'LEASE HELPUSIOiKDUCEHASTE!CXNI'ACZ'IHEIXXXlMERX'XKIBDL DESKRDCNPl-37(EXT.20079)IOEIZMQQZE%SRMIMEPBCHDIPX%UEOTIGR LISTSMRDOCUMENIS YOUDCRPTNEED)TOTALNUMBEROFCOPIESREQUIRED:

LTTR29ENCL29 0-e P.O.Box14000, JunoBeach,FL33408-0420 FEBRUARY15$999L-90-5310CFR50.36U.S.NuclearRegulatory Commission Attn:DocumentControlDeskWashington, D.C.20555Gentlemen:

RE:St.LucieUnits1and2DocketNos.50-335and50-389Monthl0eratinReortAttachedaretheJanuary1990Operating StatusandSummaryofOperating Experience ReportsforSt.LucieUnits1and2.Verytrulyyours,D.A.erVicesidentSt.LucePlantDAS/DMBAttachments cc:StewartD.Ebneter,RegionalAdministrator, RegionII,USNRCSeniorResidentInspector, USNRC,St.LuciePlant9002260449 g0013iPDRADOCK05000335RPNUanFPLGroupcompany lIPIi(f

~~AVERAGEDAILYUNITPOWERLEVELDOCKETNO.50-335UNITSt.Lucie1DATEFebruar151990COMPLETED BYD.M.BonettTELEPHONE 407694-4432MONTHZanua1990DAYAVERAGEDAILYPOWERLEVEL(MWe-Net)

~,1/1/901/2/901/3/90l/4/90il5/901/6/90il7/90l/8/901/9/90l/18/901/11/901/12/901/13/901/14/901/15/90l/16/901/17/901/18/901/19/90l/28/90l/21/901/22/90l/23/901/24/901/25/901/26/901/27/901/28/90l/29/90l/38/901/31/9085885886386784276586986886686483677886887887886886686586386185932-19-20-12-4-3-3-3-3-3 OPERATING STATUSQF'ERATIHG DATAREPORTDQCI(ETNO50-335DATE2/15/9()COMPLETED BYDoN+BQHI=TT,TELEPHONE 4<)7/694/4432 UNITNAMElST.LUCIEUNIT12.RI=PQRTING PERIOD+J*NUARYl9903iLICENSEDTHERMALPOWER<NHT)o27004+HAMI=PLATE RATING(GROSSMWE)i8585iDESTGHELECTRICAL RATING(HETMHE)+8386MAXTNUMDEPENDABLE CAF'ACXTY (GROSSNHE)l8727+MAXIMUMDEPFHDABLE CAP*CXTY(NETMHE)o8398,IFCHANCESOCCURIN,CAPACITYRATINGS(ITENSNUMBER3THROUGH7)SINCELASTREF'QRT~GIVERFASONSlPOHERLEVELTORHXCI-IRESTRICTED

~IFANY(NETMHE)10,REASONSFORRESTRXCTXONSr IFAMYL'ONTHLY

-YTD-CUMULATIVE iiiI-IOURSIHREPORTPERIOD)12.NUMBEROFHOURSRE*CTORHASCRXTICAL13,REACTQIRESERVESHUTDOWNHOURS14'OURSGENERATOR ON-LINE15'NITRI=SERVESHUTDOWNHOURS16.GROSSTHERMALENERGYGENERATED (MHH)17.GROSSELECTRIC*L ENERGYGENERATED (MWH)18HETELECTRICAL ENERGYGENERATED

<MHH)19.UNITSERVICEFACTOR28iUNXT*VA'ILABILXTY FACTOR21.CAF'ACXTY FACTOR(USIHGMDCNET)22,CAF'ACITY FACTOR(USINGDERNET)23.UNITFORCEDOUTAGERATE24'HUTDOWNS SCI.IEDULED OVERNEXT6NQHTHS1/22/907REFUEIING7445er,o0+0586+90+0l34885545431042909368+1688+769+5Zt3744507i0OiO586i90+0134885545431042909368+168ii68+769+5Zt3'114960i087895+6.ZeS387143+939+3224306495 7389738069827958875+875i674+33+525XFSHUTDOWNATENDOFRFPORTI='ERIOD~ESTIMATED DATEOFSTARTUI=':

4/21/90

UNITSHUTDOWNS ANDPOWERREDUCTIONS REPORTMONTHJanuar1990DOCKETNO.UNITNAMEDATEFebruar15,1990COMPLETED BY0.M.BonettTELEPHONE DateTypeDuration(Hours)Reason~MethodofShuttingDownReactorLicenseeEventReport¹SystemCode4Component Code~Cause&Corrective ActiontoPreventRecurrence Ol90012212.1CCHTEXCHUnit1wasshutdowntorepairatubeleakinthe1BSteamGenerator.

02900122225.0RCFUELXXDuringtheinvestigation intothe1BSteamGenerator leak,adecision-:was madetobeginthescheduled refueling andmaintenance outage.FForcedSScheduled 2ReasonA-Equipment Failure(Explain)

B-Maintenance orTestC-Refueling D-Regulatory Restriction E-OperatorTraining&LicenseExamination F-Administrative G-Operational Error(Explain)

H-Other(Explain)

Method1-Manual2-ManualScram3-Automatic Scram4-Continued 5-LoadReduction 9-Other(Explain)

ExhibitG-Instructions forPreparation ofDataEntryScheetsLicenseeEventReport(LER)

File(NUREG-0161)

Exhibit1-Same Source SUMMARYOFOPERATING EXPERIENCE DOCKETNO.50-335UNITSt.Lucie1DATEFebruary15,1990COMPLETED BYD.M.BonettTELEPHONE 407694-4432REPORTMONTHZanua1990Unit1wasshutdowntorepairatubeleakinthe1BSteamGenerator.

Duringtheinvestigation intothe1BSteamGenerator leak,adecisionwasmadetobeginthescheduled refueling andmaintenance outage.Inaccordance withrequirements ofTechnical Specification 6.9.1.6,therewerenochallenges tothePORVsorsafetyvalvesduringthereportperiod.

AVERAGEDAILYUNITPOWERLEVELDOCKETNO.50-389UNITSt.Lucie2DATEFebruar151990COMPLETED BYD.M.BonettTELEPHONE 407694-4432MONTHZanua1990DAYAVERAGEDAILYPOWERLEVEL(MWe-Net) 1/1/901/2/901/3/901/4/901/5/90l/6/901/7/901/8/901/9/90l/ie/901/11/901/12/901/13/901/14/901/15/901/16/901/17/901/18/901/19/901/ze/9e1/Zi/901/Z2/9e1/Z3/901/24/901/25/90l/26/901/27/901/28/90l/Z9/90l/3e/9e1/31/90856828716597-24-9-9-9-9-9-11-I4-26-13-3414459877285785985985185986e86e85986086e860861859 OPERATXNG STATUSOPERATXNG DATAREPORTDOCI(ETNQ50-389DATE2/l5r9eCOMPLETED BYD,M,BQNETTTELEPI.IONE 4e71'694/4432 ioUNXTNAMEiSTiLUCXEUNXT22,RI=PORTXNG PERXOD:JANUARY199e3,LXCENSEDTHERMALPOWER(MWT)'7ee 4iNAMEPLATE RATXNG(GROSSMWE)+8505+DESXGNELECTRXCAL RATTNG(NETMWE)+83ebiMAXXMUMDEPFNDABLE CAPACITY(GROSSMWE)e8827iMAXXMUMDEPENDABLE CAPACITY(NETMWE)o8398XFCHANGESOCCUI'NCAPACXTYRATXNGS(XTEMSNUMBER3THROUGI-I 7)SXNCELASTREPORTGIVEREASONS:'9iPOWERLEVELTOWKXCI-IRESTRXCTEDr XFANY(NETMWE)ie.REASONSFORRESTRXCTXONSr XFANY:MONTHLY-YTD-CUMULATXVE iiiHOURSXNREPORTPERXQD:1Z,NUMBERQFI-IOURSREACTORWASCRXTXCAL13,REACTORRESERVESHUTDOWNHOUI'S14.I.IOURSGENERATOR QN-LXNE15.UNXTRESERVESHUTDOWNHOURSiboGROSSTHERMALENERGYGENERATED (MWH)17,GROSSELI=CTRXCAL ENERGYGENERATED (MWH)18'ETELECTRXCAL ENERGYGENERATED (MWH)19,UNXTSI=RVXCEFACTORzeoUNXTAVAXLABXLXTY FACTORZi,CAr-ACXTV FhCTQR(USXNGMDCNET)22,CAPACXTYFACTOR(USXNGDERNET)23UNXTFORCEDOUTAGERATE24oSHUTDOWNS SCI.IEDULED OVERNEXT6MONTI.IS744e4eie465zeie119123739836037191162+562+559ibbe+237t57445e4i5eie465izeie1191237398360371911bzi5bzi55'9+6benz37t556857+e48673+4ewe47819i9ewe124988633 416502703938502584+184+184ib84i45i825.XFSHUTDOWNATENDOFREPORTPEI"XODESTXMATED DATEOFSTARTUP:

UNITSHUTDOWNS ANDPOWERREDUCTIONS REPORTMONTHJanuar19TELEPHONE DOCKETNO.UNiTNAMESt.Luc1e¹2DATEFebruar15,1990COMPLETED ByD.M.BonettNo.DateType'uration (Hours)Reason~MethodofShuttingDownReactorUcenseeEventReport¹SystemCode4Component CodesCause8cCorrective ActiontoPreventRecurrence 0190010402900114239.50.0N/AN/ACBVALVEXWGINSTRUUnit2wasshutdownforminorleakrepairstotwovalvesinthepressurizer cubiclearea.Duringthereturntopower,following therepairofthepressurizer valves,theunitwasheldatapproximately 205powerduetoaproblemwiththeMainFeedwater Regulating ValveLevelTransmitter LT-9011.0390011439.3.50-389-90-01 WGMECFUNDuringthereturntofullpower,thereactorwastrippedduetoanoperatorerror.Whileoffline,aproblemwiththe2CAuxiliary Feed-aterGovernorValvewasinvestigated andrepaired.

FForcedSScheduled 2ReasonA-Equipment Failure(Explain)

B-Maintenance orTestC-Refueling D-Regulatory Restriction E-OperatorTraining&UcenseExamination F-Administrative G-Operational Error(Explain)

H-Other(Explain)

Method1-Manual2-ManualScram 3-Automatic Scram4-Continued 5-LoadReduction 9-Other(Explain) 4ExhibitG-Instructions forPreparation ofDataEntryScheetsLicenseeEventReport(LER)

File(NUREG4161)

Exhibit1-SameSource IJ UNITSHUTDOWNS ANDPOWERREDUCTIONS REPORTMONTHJanuar1990DOCKETNO.UNrrNAMEStDATEFebruar151990COMPLETED BYTELEPHONE DateType'uration (Hours)Reason2MethodofShuttingDownReactorUcenseeEventReportitiSystemCode4Component CodesCause&Corrective ActiontoPreventRecurrence 04059001169001160.00.0N/AN/AHATURBINHJPUt1PXXTheascenttofullpowerwasresumedfollowing aturbineperformance test.Unit2washeldatapproxifhately 70Kpowerfortherepairofthe2ATurbineCoolingWaterPumpMechanical Seal.Fullpoweroperation wasresumed.FForcedSScheduled ReasonA-Equipment Failure(Explain)

B-Maintenance orTestC-Refueling D-Regulatory Restriction E-OperatorTraining&LicenseExamination F-Administrative G-Operational Error(Explain)

H-Other(Explain)

Method1-Manual2-ManualScram 3-Automatic Scram4-Continued 5-LoadReduction 9-Other(Explain) 4ExhibitG-instructions forPreparation ofDataEntryScheetsLicenseeEventReport(LER)

File(NURE&0161)Exhibit1-Same Source Hlt~I' SUMMARYOFOPERATING EXPERIENCE DOCKETNO.50-389UNITSt.Lucie2DATEFebruar151990COMPLETED BYD.M.BonettTELEPHONE 407694-4432REPORTMONTHZanua1990Seethe"UnitShutdowns andPowerReductions" sheetfordetails.Inaccordance withrequirements ofTechnical Specification 6.9.1.6,therewerenochallenges tothePORVsorsafetyvalvesduringthereportperiod.