ML20009G017

From kanterella
Revision as of 11:40, 15 March 2020 by StriderTol (talk | contribs) (StriderTol Bot change)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
LER 81-092/03L-0:on 810530,auxiliary Feedwater Flow Rate Instrumentation Pegged High.Caused by Failed Transmitters. Transmitters Replaced & Calibr.Power Supply Removed & Will Be Replaced
ML20009G017
Person / Time
Site: McGuire Duke Energy icon.png
Issue date: 06/25/1981
From: Nardoci P
DUKE POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20009G016 List:
References
LER-81-092-03L, LER-81-92-3L, NUDOCS 8108030245
Download: ML20009G017 (1)


Text

. ..

NMC PoRM 364 U. 3. NUCLEAR R EGULATORY COMMISSION mm LICENSEE EVENT REPORT EXHIBIT A coNTnot Stocr.: I l l l l l l (PtEAss paint on Tvre ALL mEoVI AED INFORMAT1oNI i .@

FTil r .I .N i .cl Mi ccou.

uco.su I S I Il@3.l 0101 -1 OIO

i. uca s.a I 010na 1013 E 19 23 IMI.s _11 uco.u 111n.l ll@l,a s carI s.@ l con'T M "1*c! 00LL.)@l015101010 s

en 13 I 6 I 9es @l0 oocut.f nuusan se l 5131 Ol 8 l 1 @l:s 01 mercar EvemT Cart 74 61215 O AT E l8 l140l@

EVENT oESCRIPT1oN ANo PRoSASLE CoNSECUENCES O'o ,

I o 12 I I On May 30, 1981 at 2000 hours0.0231 days <br />0.556 hours <br />0.00331 weeks <br />7.61e-4 months <br />, Unit I was entering Mode 3 from Mode 4.' The ,

AI S/G "D" Auxiliary Feedwater. Flow Rate Instrumentation was pegged-high, hence,,

AI the instrument was declared inoperable.per Technical Specification.3.3.3.6 I ITTTl I which is reportable per Technical Specification 6.9.1.13(b). The inoper-  ;

lo is t I ability of these instruments would not affect the auxiliary feedwater sys ,

L a_j r j l tem in providing and maintin.ng its.necessary functions. Therefore, the  ;

health and safety of .the public were not affected by. this . incident.  ;

e .I 7 8 nm. CAun cAv., a Co06 cCoE susCODE CDuroMEMr cQDE sua chg O's s 1oisl IIlDl@ lEl@

@ l I IN l S I T l Rl Ulg g g

~

niar vu. '.'M"r", ^,' c:g,"act aagr a a'aoa-n ,

@ ,,"u,,ma g," l-l I nl o 12 I I 013 l

- l25 8l221 l 22 2+  :-

l/l lLl 2.

[.--l l0 l 3 22 E oN b4NT ,,oyMg 's 8 0 7em 8

  • EM ' um p a hb b b b ,l, O I 0 ! 0 l 0 l @ lNl@

" lLl@

" l" R b !6 19 "l @

cAuSE oEsemirmeN ANo connEenvE Ac ious @

LL.L_J l The S/G "D" Auxiliary Feedwater Flow Monitoring Instrumentation.became in- ,

EI coerable due to failed transmitters. One transmitter (Rosemount, Model ,

LL.Lij l 1151) was sending a faulty 74 milliamp signal; and another transmitter ,

Ii12i I (Barton 386A) had burned resistors due to its power supply. Both transmitter;s mI were replaced and calibrated, and the power. supply was removed.and will be ,

2 *

  • replaced.e c._

l s ciurv as ugywoo e, FAM  % DER orMER STATUS. Osscov tRv DiscovtRY QEscn PTioM L'J.1J (_X.j@ l 0 l 01 Ol@l Mode 3 [~ l._d@l Personnel Observation l

  • c'nviry co'Irint " *
  • l an sAse LsAn Aucunro,.cnviry NA @l NA toe,no, e, ,,t,,, @

liI5Il'Zl@oo*a:Q'*l

..- .=et eno 0es l

    • so y

Nb A TvPf ogsCMspTtCM l'1711010lOl@[Z_J@l NA  ;

noso~~e't inw',? as io

-u . anc.,,no~@

18181 l 0 l O l0atl@la2 NA I 8 9 l L C8 cA O.M.ct To p.CluTY 30 EDDs LZJ@l NA 7 t to l

rusucirv to 4 NAC U$( eN(y issuto ot scairrion A Ls.J

' = '

6 l'= NA l (([ti;;;;;;;[

n ., ,.

NAME CF PREPARER Phillip B. Nardoci ,weur; (704) 373-7432 8108030245 810625 PDR ADOCK 05000369 S PDR

_- .