ML18227A417

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Attached October, 1977 Operating Status Reports for Turkey Point Unit Nos. 3 & 4 and St. Lucie Unit No. 1
ML18227A417
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 11/05/1977
From: Schmidt A
Florida Power & Light Co
To:
Office of Nuclear Reactor Regulation
References
Download: ML18227A417 (13)


Text

NRC FoRM 195 (2 78)

U.S. NUCLEAR REGULATORY COMMISSIO 0-DOCKET NUMBER FILE NUMBER 25 NRC DISTRIBUTION FoR PART 50 DOCKET MATERIAL IeNTHL TO: FROMI DATE OF OOCUMENT Florida Power 6 Light Company ll/S/77 /

Hi Ri Co Miami, Florida OATE RECEIVED I Ai Di Schmidt ll/ll/77 QLETTER Q NOTOR IZE O ,

PROP INPUT FORM NUMBER OF COPIES RECEIVEO Q OR IG INAL QUNCLASSIFIE 0 QCOI V DESCRIPTION Letter trans the f'ollowing.'NCL.OSURE Month~ Report l;or October'977 Plant & Component Operability &, Availability.

Thi.s Report to be used in preparing Gray Rook by PlanS h Operations.

(1-P) (9-P)

PLANT QME Turkey Point Units 3 8 4 Sti Lucie Unit 1 RJL 11/14/77 FOR ACTION/INFORMATION INTERNAL D ISTR I BUTION nc e EXTERNAL DISTRIBUTION CONTROL NUMBER

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/ lv0103 NRC FORM 19d I2 7d)

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FLORIOA POWER & LIGHT COMPANY November 5, 1977 Office of Management, Information and Program Controls U. S. Nuclear Regulatory Commission Nashington, D. C. 20555 Gentlemen:

Attached are the October, 1977, Operating Status Reports for Turkey Point Unit Nos. 3 and 4 and St. Lucie Unit No. 1.

Very truly yours, D. Schmidt Vice President Power Resources VTC/DDC cc: Mr. James P. O'Reilly Robert Lowenstein, Esquire 77n1 ~rr01 Qe PEOPLE... SERVING PEOPLE

0 APPENDIX B AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.

Turkey Point UNIT Unit No. 3 DATE COMPLETED BY V. T. Chilson TELEPHONE (305) 552-3824 MONTH OCTOBER 1977 DAY AVERAGE DAILY POWER .LEVEL DAY AVEBAGE DAILY PO~ LEVEL I (Nfe-Net) (MWe-Net) 593 17 622 629 18 623 3 636 19 618 639 20 5 639 21'2 620 635 620 636 622 637 24 618 639 25 615 10 637 26 615 632 27 615 12 573 28 610 13 624 29 615

'4 625 30 632 15 625 633 16 624

OPFRATING DATA REPORT DOCKET NO.

DATE Kg~~77 COhiPLETED BY >-T. Chilson TELEPHONE ~305 552-3525 OPERATING STATUS Notes

1. Unit Name:
2. Reportfng Period: October 1977
3. I.icensed Thermal Power (MWt):
4. Nameplate Rating (Gross MWe):
5. Design Electrical Rating (Net MWe):
6. Maximum Dependable Capacity (Gross MWe):
7. Maximum De p endable Ca p acit y(Net MWe: )
8. IfChanges Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Give Reasons:
9. Power Level To Which Restricted, IfAny (Net MWe): NO.
10. Reasons For Restrictions, If Any:

This Month Yr:to-Date Cumulative I

11. Hours In Reporting Period 7 296.0 43'17..6
12. Number Of Hours Reactor Was Critical 633.0 34 673.1 13, Reactor Reserv~ Shutdown Hours 43.7 ill.2.

'4. 743.8 6 495. 0 33" 534;1 Hours Generator On-Line 85.0

16. Gross Thermal Energy Generated (MWH) 1 628 892 13 960 533 65 690 121 489 515 386 811 20 957 262
17. Gross Electrical Energy Generated (MWH)
18. Net Electrical Energy Generated (hIWH)
19. Unit Service Factor
20. Unit Availability Factor' 464 396 99.8 99 ~ 8 .

89 89.0

..0'7..

4 163 971' " 19'39 78.1 906 9

21. Unit Capacity Factor (Using MDC Net) 85.7 70.1
82. 4 '66.5 0.2, 2.6 2.9'
23. Unit Forced Outage Rate
24. Shutdowns Scheduled Over Next 6 Months (Type. Date. and Duration of Each)

Refuelin maintenance and ins ections - Hov. 19 1977 Jan. 16. 1978

25. IfShut Down At End Of Report Period, Estimated Date of Startup:
26. Units In Test Status (Prior to Commercial Operation): Forecast Achieved INITIALCRITICALITY INITIALELECTRICITY COhlMERCIAL OPERATION

.) REASON APPENDIX D DOCKET NO. 50 - 250 A: +UIPHEHT FAILURE (EXPIAIH) Turkey Point B: Eihiiff. OR TEST UNIT SHUTDOWNS AND POWER REDUCTIONS UNIT NAEIE Unit Ho. 3 C: REFUEI.IHC D: REGULATORY RESTRICTIOH DATE Nov. 5 1977 E: OPCRATOR TRAIHINC AND I.ICEHSE EXAMIHATIOH COHPI.ETED BY V. T. Chilson F: ADIIINISTRATIVE -

C: OPERATIONAL ERROR (EXPIAIN) REPORT HONTN OCTOBER, 1977 TELEPHONE (305) 552 3824 H: OTHER (EXPIAIN)

) EIETNOD 1: HANUAI, . HETHOD OF 2: EIANUAI. SCRAH TYPE S)EUTTINC DOWN 3: AUTOHATIC SCRAH F: FORCED DURATION THE REACTOR OR 4: 01 IIER (EXPIAIN) NO. DATE S: SCHEDULED (IIOURS) REASON(1) REDUCIHC POWER(2) CORRECTIVE ACTIONS/COEIMENTS 25 77-10-12 1.2 Unit trip caused by malfunction of the generator voltage regulator. Corrective actions included repairing a faulty component in the voltage regulator control system. (Hon-nuclear system)

SUMMARY

Unit No. 3 operated at approximately 100X R.P., except for outage on Scptembcr 12, 1977.

0 I

APPENDIX B AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50 251 Turkey Point UNIT Unit No. 4 DATE Nov. 5 1977 COMPLETED BY V. T. Chilson TELEPHONE (305) 552-3824 MONTH OCTOBER, 1977 DAY AVERAGE DAILY POWER. LEVEL DAY AVERAGE DAILY PO~ LEVEL (MWe-Net) (MWe-Net) 658 17 668 657 18 671 3 652 19 665

~

4 655 20 665 5 672 21 665 675 22 666 673 672 674 24 62 670 25 647 10 664 26 648 658 27 647 12 658 28 269 657 . 29 14 670 30 674 31 16 670 VaOTE: Average daily power greater than 666 MÃe due to cooler condenser cooling water.

OP~cTING DATA REPORT DOCKET NO.

D4TE Hov. 5 1977 C051PLETED BY ~V. Chllson TELEFHOHE ~30 552-3524 OPERATING STATUS Notes

] Unit Name Turke Po U 1 o

2. Reporting period: October 1977
3. Licensed Thermal Power (MWt):

s

4. Namephte Rating (Gross MWe):
5. Design Electrical Rating (Net MWe):
6. Maximum Dependable Capacity (Gross MWe):
7. Maximum Dependable Capacity (Net hWe) t
8. IfChanges Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:

IfAny (Net MWe): NONE

9. Power Level To Which Restricted,
10. Reasons For Restrictions, IfAny:

s This Month Yr:to.Date Cumulative ..

11. Hours In Reporting Period

' 45. 7 296.0 36'45.0

12. Number Of Hours Reactor Was Critical 659.3 4 553.3 26 275.0
13. Reactor Reserve Shutdown Hours 438.8:-
15. Unit Reserve Shutdown Favours 16.'ross Thermal Energy Generated (MWH) 1 443 071 457 595 3 049 807 17 007 490

'620

'7.9

17. Gross Electrical Energy Generated (MWH) 435 282 ' 890 520 &86
18. Net Electrical Energy Generated (MWH)
19. Unit Service Factor 60..4 67.. 9
20. Unit Availability Factor 60.4

,21. Unit Capacity Factor (Using MDC Net) 59.5 66.5

23. Unit Forced Outage Rate 2.4 3.4
24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):

s

25. IfShut Down At End Of Report Period, Estimated Date nf Startup:

Nov. 11, 1977

26. Units In Test Status (Prior to Commercial Operation): Forecast Achieved INITIALCRITICALITY INITIALELECTRICITY COMMERCIALOPERATION (9/77)

APPEtiDIX D DOCKET tlo.

.) REASotl Turkey Point h: EQUIPHEHT FAII.URE (EXPLAIN) UNIT SIIUTIMMHS AND POIIER REDUCTIONS UNIT NAHE Unit Ho. 4 B: HhltlT. OR TEST C: REFUEI.IHG DATE Nov. 5 1977 D: REGUIATOIIY RESTRICTION E: t)l'ERATOR TRAIHIHG AHD COHPIZTED BY V. T. Chilson LICFNSE EXAHINATIOH F: AIIHINISTRATIVE TELEPHONE (305) 552-3824 G: OPERATIOHAI. ERROR (EXPLAIN) REPORT HOHTII OCTOBER. 1977 II: OTHER (FBPLAItl)

) tlETIIOD I: HAtlUAL . HETNOD OF 2: HAHUAL SCRAII TYPE SNUTTIHG DOMN 3- AUIYIIIATICSCRAII Fi FORCED DURATION THE REACTOR OR 4: OTIIER (EXPLAIN) HO. DATE 8: SCIIEDULED gIOURS) REASON(1) REDUCING POMER(2) CORRECTIVE ACTIONS/COHHEHTS 16 77-10-28 86.0 Unit was removed from service to locate and repair tube leak in steam generator No. 4B. Corrective actions included plugging one leaking tube. (Huclear system)

SUHHARY: Unit No. 4 operated at approximately 10OX R.P. until October 28, 1977, when the unit was removed from service to repair steam generator No. 4B tube leak.

APPENDIX B AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50 335 St. Lucie UNIT Unit No.'

DATE Nov. 5, 1977 COMPLETED BY V. T. Chilson TELEPHONE (305) 552-3824 MONTH OCTOBER 1977 DAY AVERAGE DAILY POWER .LEVEL DAY AVERAGE DAILY POtPuR L VEL (Nfe-Net) (MRe-Net) 17 789 18 791 3 19 791 20 779 21 763 22 792 793 24 770 25 790 10 232 26 790 740 27" 776 12 773 28 .

652 13 785 29 666 14 787 30 754 789 31 686 16 789 NOTE: Average daily power greater than 777 MWe due to cooler condenser cooling water.

OPERATING DATA REPORT DOCKET NO.

DATE 3hz '~977 COMPLETED BY TELEPHONE 3LZ

~305

~son 552-3824 OPERATING STATUS St. Lucie Unit No. 1 Notes I Umt Name:

2. Reportmg Period: Oct:ober 1977
3. Licensed Thermal Power (44IWt) t
4. Namephte Rating (Gross hIWe):
5. Design Electrical Rating (Net MWe):

22

7. Maximu m De pe ndable Ca p acit y(Net MWe: 777

)

8. IfChanges Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:

IfAny (Net MWe): NONE

9. Power Level To Which Restricted,
10. Reasons For Restrictions, If Any:

~

~ I ~ ~

11. Hours In Reporting Period
12. Number Of Hours Reactor Was Critical

'45. This Month 0

523 ~ 3 Yr.-to-Date 6 182.5 1

Cumulative .

7 6

560.0 446.5

13. Reactor Reserve Shutdown Hours
15. Unit Reserve Shutdown E3ouzs JlilL -0'-

101;5.

.'101.5

17. Gross Electrical Energy Generated (MWH) 414 4 502 280 4 610 550

'4 ' 4" 322'96

18. Net electrical Energy Generated (hIWH) 390 160 223 721
20. Unit Availability Factor 69.4 . 81;8 82.4
21. Unit Capacity Factor (Using MDC Net) 67.4 73.6 ..

Unit Forced Outage Rate I>>'3.

12.3 11.

24. Shutdowns Scheduled Over Next 6 hlonths (Type. Date, and Duration of Each): ~

9'97&

Refuelin maintenance and ins ections March 15 June 6

25. If Shut Down At End Of Report Period. Estimated Date of Startup:
26. Units In Test Status (Prior to Commercial Operation): Forecast Achieved INITIAL CRITICALITY INITIAL ELECTRICITY COhlhIERCIAL OPERATION (oI77)

APPENDIX D DOCKET NO. 50 - 335

) REASON St. Lucis A: EqUIPNL'NT FAILURE (EXPLAIN)

UHIT SllUTDOWNS AND POWER REDUCTIONS UNIT HAHE Unit No. 1 B: HAINT. OR TIST C RL'FUbl IN( DATE Nov. 5 1977 D: REGULATORY RESTRICTIOH E: OPERATOR TRAINING AND COHl LETED BY V. T. Cbilson LICENSE EXAHINATION F: ADNIHISTRATIVE TELEPHONE (305) 552"3824 C: OPERATIONAL ERROR (EXPLAIN)

H: OTHER (FAPLAIN)

) HETIIOD I: HAHUAL . HETHOD OF SllUTTINC DOWN 2: HANUAL SCRAH TYPE 3: AUTOHATIC SCRAH F: FORCED DURATION THE REACTOR OR 4: OTHER (EXPLAIN) HO. DATE S: SCHEDUr.ED (HOURS) REASON(1) REDUCINC POWER(2) CORRECTIVE ACTIONS/COtlHEHTS 33 77-09-24 228.0 Unit was removed from service to perform preliminary warranty inspection. (Continued from previous montb)

(Nuclear and non-nuclear systems)

SUHHARY: Unit was returned to service on October 10, 1977, following completion of scheduled outago to perform preliminary warranty inspection.