IR 05000454/2006004
ML063120614 | |
Person / Time | |
---|---|
Site: | Byron ![]() |
Issue date: | 11/08/2006 |
From: | Richard Skokowski NRC/RGN-III/DRP/RPB3 |
To: | Crane C Exelon Generation Co, Exelon Nuclear |
References | |
FOIA/PA-2010-0209 IR-06-004 | |
Download: ML063120614 (60) | |
Text
November 8, 2006 Mr. Christopher President and Chief Nuclear Officer
Exelon Nuclear
Exelon Generation Company, LLC
4300 Winfield Road
Warrenville, IL 60555SUBJECT:BYRON STATION, UNITS 1 AND 2 NRC INTEGRATED INSPECTION REPORT 05000454/2006004; 05000455/2006004
Dear Mr. Crane:
On September 30, 2006, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated inspection at your Byron Station, Units 1 and 2. The enclosed report documents the
inspection findings which were discussed on October 03, 2006, with Mr. Dave Hoots and other
members of your staff.
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed
personnel.
This report documents three NRC-identified findings of very low safety significance (Green). All three findings involved violations of NRC requirements. In addition, two licensee-identified
violations which were determined to be of very low safety significance are listed in this report.
However, because of the very low safety signi ficance of the violations and because they were entered into your corrective action program, the NRC is treating these violations as non-cited
violations (NCVs) consistent with Section VI.A.1 of the NRC Enforcement Policy.
If you contest the subject or severity of a Non-Cited Violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the
U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, D.C.
20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission -
Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of
Enforcement, U.S. Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the
Resident Inspector office at the Byron facility.
C. Crane-2-In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be made available electronically for public inspection in the NRC
Public Document Room or from the Pub licly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA PLouden acting for/
Richard A. Skokowski, Chief Branch 3 Division of Reactor Projects Docket Nos. 50-454; 50-455 License Nos. NPF-37; NPF-66Enclosure:Inspection Report 05000454/2006004; 05000455/2006004; w/Attachments 1: Supplemental Information 2: Confirmatory Measurements Comparison Chart
3: Tritium Sample Resultscc w/encl:Site Vice President - Byron Station Plant Manager - Byron Station
Regulatory Assurance Manager - Byron Station
Chief Operating Officer
Senior Vice President - Nuclear Services
Vice President - Mid-West Operations Support
Vice President - Licensing and Regulatory Affairs
Director Licensing
Manager Licensing - Braidwood and Byron
Senior Counsel, Nuclear
Document Control Desk - Licensing
Assistant Attorney General
Illinois Emergency Management Agency
State Liaison Officer, State of Illinois
State Liaison Officer, State of Wisconsin
Chairman, Illinois Commerce Commission
B. Quigley, Byron Station
SUMMARY OF FINDINGS
IR 05000454/2006004; 05000455/2006004; on 07/01/2006-09/30/2006; Byron Station, Units 1 and 2; Fire Protection; and Radiation Protection.
This report covers a 3-month period of baseline resident inspection and announced baseline inspections on Radiation Protection and Temporary Instruction (TI) 2515/166, "Pressurized
Water Reactor Containment Sump Blockage." These inspections were conducted by four regional inspectors and the resident inspectors. Three Green findings, all of which were non-
cited violations (NCV), were identified. The significance of most findings is indicated by their color (Green, White, yellow, Red) using Inspection manual chapter (IMC) 0609, "Significance
Determination Process" (SDP). Findings for which the SDP does not apply may be "Green" or be assigned a severity level after NRC management review. NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor
Oversight Process," Revision 3, dated July 2000.A.Inspector-Identified and Self-Revealed Findings
Cornerstone: Mitigating Systems
- Green.
The inspectors identified a Non-Cited Violation of Byron Facility Operating License Nos. NPF-37 and NPF-66, Condition 2.c.6, for failing to maintain the firewall separating the Auxiliary Building from the penetration area in accordance with the approved fire protection program. Fire seals were required to be provided in this firewall, except where an evaluation had been perfo rmed and approved to allow a deviation.
Two sleeves containing fire seals had pulling ropes embedded in the fire seals in the firewall separating the Auxiliary Building General Area 401 from the Unit 1 piping penetration area; also, no evaluation or exemption existed to justify this configuration.
The licensee entered the issue into its corrective action program for resolution and implemented compensatory measures that included hourly fire watches.
This finding was more than minor because it affected the Mitigating Systems Cornerstone objective to ensure that external factors (i.e., fire, flood, etc) do not impact the availability, reliability, and capability of systems that respond to initiating events. The finding was of very low safety significance because the fire seals were in small diameter sleeves that traveled a distance of 45 feet and had two 90 degree bends and the location of combustibles were positioned such that the piping penetration end of the fire seals would not be subject to direct flame impingement. (Section 1R05)
Cornerstone: Occupational Radiation Safety
- Green.
An inspector-identified finding of very low safety significance and two associated Non-Cited Violations of NRC requirements were identified for the failure to post and control access to High Radiation Areas, as required by 10 CFR Part 20, to notify individuals of the radiological hazard present and to prevent the unauthorized entry to such areas. Specifically, the entrance to the Unit 1 Filter Valve Aisle located on the 383'
elevation of the Auxiliary Building, a high radiation area with a radiation dose rate of approximately 135 millirem in one hour, was not posted or controlled by any of the methods described in 10 CFR 20.1902, 10 CFR 20.1601, or Technical Specification 5.7.1.
The issue was more than minor because the issue was associated with the Program/Process attribute of the Occupational Radiation Safety Cornerstone and affected the cornerstone objective to ensure adequate protection of the worker health and safety from exposure to radiation from radioactive material during routine civilian nuclear reactor operation. The issue represents a finding of very low safety significance because the finding did not constitute an ALARA or work control issue, did not result in an overexposure or the substantial potential for an overexposure, and did not compromise the licensee's ability to assess dose. Non-Cited Violations of 10 CFR 20.1902 and 10 CFR 20.1601 were identified for the failure to post and control access to high radiation areas. Corrective actions taken by the licensee for this finding included establishing control through postings and barricades. The cause of this finding is related to the cross-cutting element of human performance. (Section 2OS1).
Cornerstone: Public Radiation Safety
- Green.
An inspector-identified finding of very low safety significance and an associated Non-Cited Violation of NRC requirements were identified for the failure to perform surveys that are necessary to comply with the regulations in 10 CFR Part 20 and that are reasonable under the circumstances to evaluate the extent of radiation levels, concentrations or quantities of radioactive materials, and the potential radiological hazards that could be present prior to pumping liquids from blowdown line vacuum breaker valve vaults to the environment.
Specifically, the conditions found at 0CW276 (vault No. 6) on July 7, 2005, were outside the parameters of the original assessment, and the licensee did not evaluate the change of conditions for the potential radiological hazards to ensure compliance with 10 CFR 20.1301, which limits radiation exposure to a member of the public to 0.1 rem.
The issue was more than minor because the issue was associated with the Program/Process attribute of the Public Radiation Safety Cornerstone and affected the cornerstone objective to ensure adequate protection of public health and safety from exposure to radioactive materials released into the public domain as a result of routine civilian nuclear reactor operation. Since the releases were limited to licensee owned property, the licensee has not measured any licensed material beyond its property line, and the licensee's REMP has a monitoring well in the vicinity of the blowdown lines, the finding did not represent a failure to assess dose nor a failure to assess the environmental impact. Consequently, the fi nding was determined to be of very low safety significance. A Non-Cited Violation of 10 CFR 20.1501 was identified for the failure to make surveys to ensure compliance with 10 CFR 20.1301, which limits radiation exposure to a member of the public to 0.1 rem. Corrective actions taken by the licensee for this finding included performing surveys of the soil surrounding the vacuum breaker vault for radionuclides, establishing additional groundwater monitoring wells, sealing the vacuum breaker vaults, and inst alling of an automated leak detection system.
The cause of this finding is related to the cross-cutting element of problem identification and resolution. (Section 2PS1).
4
B.Licensee Identified Violations
Two violations of very low safety significance, which were identified by the licensee, have been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensee's corrective action program. These violations and the licensee's corrective action tracking numbers are listed in
Section 4OA7 of this report.
5
REPORT DETAILS
Summary of Plant Status Unit 1 operated at or near full power throughout the first part of the inspection period. On August 25, 2006, the unit commenced a coast down for the upcoming refueling outage. On
September 10, 2006, at 11:00 p.m. the licensee opened the main generator output breaker and
entered a planned refueling outage. At the end of the report period the licensee was still in the
outage.Unit 2 operated at or near full power throughout the inspection period with the following exception: on July 29, 2006, Unit 2 power was reduced to approximately 63% due to offsite
transmission line issues. The unit was returned to full power the following day.1.REACTOR SAFETYCornerstone: Initiating Events, Mitigating Systems, Barrier Integrity andEmergency Preparedness
1R04 Equipment Alignment
.1Partial Walkdowns
a. Inspection Scope
The inspectors performed three partial walkdown samples of accessible portions of trains of risk-significant mitigating systems equipment during times when the trains were
of increased importance due to the redundant trains or other related equipment being
unavailable. The inspectors utilized the valve and electric breaker lineups and
applicable system drawings to determine that the components were properly positioned
and that support systems were lined up as needed. The inspectors also examined the
material condition of the components and observed operating parameters of equipment
to determine that there were no obvious deficiencies. The inspectors used the
information in the appropriate sections of the UFSAR and TS to determine the functional
requirements of the systems.
The inspectors verified the alignment of the following:
- Unit 2 Emergency Core Cooling System;*Unit 1 Electrical Bus 131X; and
- Unit 2 Train A Emergency Diesel Generator.
The inspectors also reviewed selected issues documented in IRs, to determine if they had been properly addressed in the licensee's corrective action program. The
documents reviewed during this inspection are listed in the Attachment to this report.
b. Findings
6 No findings of significance were identified..2Complete Walkdown
a. Inspection Scope
During the inspection, the inspectors finished one complete system alignment inspection of the accessible portions of the Spent Fuel Pool Cooling system after Unit 1 core was
offloaded. This system was selected because it was considered both safety-related, and
risk significant for the plant condition. The inspection consisted of the following
activities:*a review of plant procedures (including selected abnormal and emergency procedures), drawings, and the UFSAR to identify proper system alignment;*a review of outstanding work requests on the system;
- a review of outstanding temporary modifications on the system;
- a review of the system health information; and
- a walkdown of the system to determine proper alignment, component accessibility, availability, and current condition.
The inspectors also reviewed selected issues documented in IRs, to determine if they had been properly addressed in the licensee's corrective actions program. The
documents reviewed during this inspection were listed in the Attachment at the end of
this report.
b. Findings
No findings of significance were identified.
1R05 Fire Protection (71111.05).1Quarterly Walkdowns
a. Inspection Scope
The inspectors conducted fire protection walkdowns that were focused on availability, accessibility, and the condition of fire fighting equipment; the control of transient
combustibles and ignition sources; and on the condition and operating status of installed
fire barriers. The inspectors reviewed applicable portions of the Byron Station Fire
Protection Report and selected fire areas for inspection based on their overall
contribution to internal fire risk, as documented in the Individual Plant Examination of
External Events Report.
The inspectors verified that fire hoses and extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were
unobstructed; that transient material loading was within the analyzed limits; and that fire
doors, dampers, and penetration seals appeared to be in satisfactory condition. The
Byron Station Pre-Fire Plans applicable for each area inspected were used by the
inspectors to determine approximate locations of firefighting equipment.
7 The inspectors completed eight inspection samples by examining the plant areas listed below to observe conditions related to fire protection:*Circulating Water Pump House (Zone 18.12-0);*Auxiliary Building Elevation 383' General Area (Zone 11.4-0);
- Auxiliary Building Elevation 401' General Area (Zone 11.5-0);
- Turbine Building 451' General Area (Zone 8.6-0);
- Unit 2 Division 21 Miscellaneous Electrical Equipment and Battery Room (Zone 5.2-2);*Unit 2 Auxiliary Electrical Equipment Room (Zone 5.5-2);
- Unit 1 Train B Diesel Generator & Day Tank Room (Zone 9.1-1 & 9.4-1); and
- Unit 1 Containment Pipe Penetration Area (Zone 11.3-1).
The inspectors reviewed selected issues documented in CRs, to determine if they had been properly addressed in the licensee's corrective action program. The inspectors
also verified that minor issues identified during the inspection were entered into the
licensee's corrective action program. The documents reviewed during this inspection
are listed in the Attachment to this report.
b. Findings
Failure to Maintain Fire Barriers in Accordance with Fire Protection Program Introduction
- The inspectors identified a Green finding and associated Non-Cited Violation of Byron Facility Operating License Nos. NPF-37 and NPF-66, Condition 2.c.6, for failing to maintain the firewall separating the Auxiliary Building from the penetration
area in accordance with the approved fire protection program.
Description
- On September 25, 2006, during a routine fire protection walkdown of the Unit 1 auxiliary building mechanical penetration room, referred to by the licensee as
Area 5, the inspectors noted that there were ropes running through fire barriers in 5 inch
diameter conduit in cable tray 1757D C1E. The inspectors notified the licensee who
performed an independent walkdown and verified the installation of unapproved material
in the fire seals. This was inconsistent with Section 2.3.11.41 of the Fire Protection
Report, which described the fire area analysis for the 401 elevation of the Auxiliary
Building and stated that rated fire barriers separate this zone from the remainder of the
plant.The inspectors reviewed the Fire Protection Report and did not identify any existing deviations allowing for the existence of this condition. The licensee entered this issue in
their corrective action program for resolution (IR 536504) and implemented
compensatory actions that included hourly fire watches. By the end of the report period
the licensee had repaired the fire seals, restoring them to operable and then suspended
the compensatory actions.
Analysis:
The inspectors determined that the licensee's failure to maintain the fire seal between fire zone 11.3-1 and fire zone 11.5-0 in accordance with the approved fire
protection program was a performance deficiency warranting a significance
determination. Furthermore, the issue was considered more than minor because the 8 finding affected the attribute of protection against external factors (i.e. fire) of the Mitigating System Cornerstone. This finding was of very low safety significance because
the fire seals were of small diameter, traveled 45 feet with two 90 degree bends and the
location of combustibles were positioned such that the piping penetration end of the fire
seals would not be subject to direct flame impingement.
Enforcement
- Byron Plant Operating License Condition 2.c.6 stated, in part, that "The licensee shall implement and maintain in effect all provisions of the approved fire
protection program as described in the UFSAR." Section 9.5.1 of the UFSAR stated that
"The design bases, system descriptions, safety evaluation, inspection and testing
requirements, personnel qualification, and training are described in Reference 1 [the Fire
Protection Report]." Contrary to the above, the licensee failed to maintain the firewall
separating the Auxiliary Building from the penetration area in accordance with the
approved fire protection program. Fire seals were required to be provided in this firewall, except where an evaluation had been perfo rmed and approved to allow a deviation.
Two sleeves containing fire seals had pulling ropes embedded in the fire seals in the
firewall separating the Auxiliary Building General Area 401 from the Unit 1 piping
penetration area; also, no evaluation or exemption existed to justify this configuration.
Because this issue was entered into the corrective action program as IR 536504, and
the finding was of very low safety significance, this violation is being treated as an NCV
consistent with Section VI.A of the NRC Enforcement Policy. (NCV 05000454/2006004-
01;05000455/2006004-01, Failure to Maintain Fire Barrier in Accordance with Fire
Protection Program).2Annual Drill Observation
a. Inspection Scope
The inspectors assessed the fire brigade performance and the drill evaluator's critique during a fire brigade drill conducted on August 31, 2006. The drill simulated a fire in the
Nuclear Station Work Permit building. The inspectors also observed an actual fire
brigade response to a fire alarm received in the Auxiliary Building on August 28, 2006.
Details of the fire response were documented in Section
4OA3 of this report.
The
documents reviewed for this portion of the inspection are listed in the Attachment to this
report.The inspectors focused on command and control of the fire brigade activities; fire fighting and communication practices; material condition and use of fire fighting
equipment; and implementation of pre-fire plan strategies. The inspectors evaluated the
fire brigade performance using the licensee's established fire drill performance
procedure criteria. An annual inspection sample was not completed in this report since
not all aspects of the inspectible areas were reviewed. Observation and evaluation of
other important drill activities designated in Section 02.02 of the inspection procedure
will be performed during subsequent observations of licensee drill activities.
b. Findings
No findings of significance were identified.
91R11Licensed Operator Requalification (71111.11).1Resident Inspector Quarterly Review
a. Inspection Scope
The inspectors completed one inspection sample by observing and evaluating an operating crew during a steam line break outside containment with failure of all MSIV's
to close. The inspectors evaluated crew performance in the areas of:*Clarity and formality of communications;*Ability to take timely actions;
- Prioritization, interpretation, and verification of alarms;
- Procedure use;
- Control board manipulations;
- Supervisor's command and control;
- Management oversight; and
- Group dynamics.
The inspectors verified that the crew completed the critical tasks listed in the above simulator guide. The inspectors also compared simulator configurations with actual
control board configurations. For any weaknesses identified, the inspectors observed
the licensee evaluators to determine whether they also noted the issues and discussed
them in the critique at the end of the session. The inspectors verified that minor issues
were placed into the licensee's corrective action program.
The documents reviewed during this inspection are listed in the Attachment to this report.
b. Findings
No findings of significance were identified.
1R12 Maintenance Effectiveness (71111.12).1Resident Inspector Quarter Review
a. Inspection Scope
The inspectors completed two inspection samples by evaluating the licensee's implementation of the maintenance rule, 10 CFR 50.65, as it pertained to identified
performance problems associated with the following structures, systems, and/or
components:*Unit 1 Train B Emergency Diesel Generator Trip During Cooldown Cycle; and*Unit 1 Molded Case Circuit Breaker Failures.
The inspectors evaluated the licensee's appropriate handling of structures, systems, and components (SSC) condition problems in terms of appropriate work practices and 10 characterizing reliability issues. Equipment problems were screened for review using a problem oriented approach. Work practices related to the reliability of equipment
maintenance were observed during the inspection period. Items chosen were risk
significant, and extent of condition was reviewed as applicable. Work practices were
reviewed for contribution to potential degraded conditions of the affected SSCs. Related
work activities were observed and corrective actions were discussed with licensee
personnel. The licensee's handling of the issues being reviewed was evaluated under
the requirements of the maintenance rule.
The inspectors also reviewed selected issues documented in CRs, to determine if they had been properly addressed in the licensee's corrective action program. The
documents reviewed during this inspection are listed in the attachment to this report.
b. Findings
No findings of significance were identified.
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)
a. Inspection Scope
The inspectors reviewed the licensee's management of plant risk during emergent maintenance activities or during activities where more than one significant system or
train was unavailable. The inspectors chose activities based on their potential to
increase the probability of an initiating event or impact the operation of safety-significant
equipment. The inspectors verified that the evaluation, planning, control, and
performance of the work were done in a manner to reduce the risk and the work duration
was minimized where practical. The inspecto rs also verified that contingency plans were in place where appropriate.
The inspectors reviewed configuration risk assessment records, UFSAR, TS, and Individual Plant Examination. The inspectors also observed operator turnovers, observed plan-of-the-day meetings, and reviewed other related documents to determine
that the equipment configurations had been properly listed, that protected equipment
had been identified and was being controlled where appropriate, and that significant
aspects of plant risk were being communicated to the necessary personnel.
The inspectors completed five inspection samples by reviewing the following activities:
- Emergent Failure of the Unit 1 Train B Emergency Diesel Generator During Monthly Run;*Unit 2 Train B Residual Heat Removal Pump Out of Service (OOS) while Unit 1 East Main Power Transformer Sensor was Replaced and while Unit 0 G train SX
Cooling Tower was OOS;*Unit 1 Train A Essential Service Water Pump Work Window while Unit 0 Essential Service Water Makeup Pump was OOS;*Emergent Schedule Change Due to Thunderstorms and the Delay in the Flood-up of the Reactor Vessel for Unit 1 with a Consequential Increase in Loss of Core
Cooling While at Reduced Inventory; and 11*Unit 2 Train A Direct Current (DC) Bus Cross-tied to Unit 1 Train A while Unit 1 Train A Emergency Diesel Generator was OOS.
The documents reviewed during this inspection are listed in the Attachment to this report.
b. Findings
No findings of significance were identified.
1R15 Operability Evaluations (71111.15)
a. Inspection Scope
The inspectors evaluated plant conditions, selected condition reports, engineering evaluations, and operability determinations for risk-significant components and systems
in which operability issues were questioned. These conditions were evaluated to
determine whether the operability of components was justified.
The inspectors completed eight inspection samples by reviewing the following evaluations and issues:*Unit 1 Train A Diesel Generator Excessive Combustion Air Moisture;*Seismic Monitoring System Ou t of Service and Impact Upon EALs;*Unit 1 Pressurizer Power Operated Relief Valve Elevated Tailpipe Temperature;
- Unit 1 Train A Containment Spray Additive System Valve Weld Leak;
- Unit 2 Train B Essential Service Water Pump Bearing Slinger Ring Not Rotating;
- Unit 2 Train B Auxiliary Feedwater Pump Jacket Water Expansion Tank Leak;
- Unit 1 Molded Case Circuit Breaker Failure; and
- Unit 1 Emergency Core Cooling System Piping Air Entrainment.
The inspectors compared the operability and design criteria in the appropriate section of the TS including the TS Basis, the Technical Requirements Manual (TRM) and UFSAR
to the licensee's evaluations to determine that the components or systems were
operable. The inspectors determined whether compensatory measures, if needed, were
taken, and determined whether the evaluations were consistent with the requirements of
licensee procedures. The inspectors also discussed the details of the evaluations with
the shift managers and appropriate members of the licensee's engineering staff.
The inspectors also reviewed selected issues documented in IRs, to determine if they had been properly addressed in the licensee's corrective action program. The
documents reviewed during this inspection are listed in the Attachment to this report.
b. Findings
No findings of significance were identified.
1R19 Post Maintenance Testing (71111.19)
a. Inspection Scope
The inspectors reviewed the post maintenance testing activities associated with maintenance or modification of mitigating, barrier integrity, and support systems that
were identified as risk significant in the licensee's risk analysis. The inspectors reviewed
these activities to determine that the post maintenance testing was performed
adequately, demonstrated that the maintenance was successful, and that operability was
restored. During this inspection activity, the inspectors interviewed maintenance and
engineering department personnel and reviewed the completed post maintenance
testing documentation. The inspectors used the appropriate sections of the TS, TRM, and UFSAR, and other related documents to evaluate this area.
The inspectors completed six inspection samples by observing and evaluating the post maintenance testing subsequent to the following maintenance activities:*Unit 1 Train A Safety Injection to Charging Pump Suction Header Cross-Tie Isolation Valve Actuator Rebuild;*Unit 1 Train A Emergency Diesel Generator valve work;
- Unit 1 Train A Essential Services Water Pump oil cooler inspection;
- Unit 1 Train B Centrifugal Charging Pump Work Window;
- Unit 0 Train B Essential Service Water Makeup Pump Work Window; and
- Unit 1 Division 11 DC Bus Circuit Breaker Change-out.
The inspectors also reviewed selected issues documented in CR's to determine if they had been properly addressed in the licensee's corrective action program. The
documents reviewed during this inspection are listed in the Attachment to this report.
b. Findings
No findings of significance were identified.
1R20 Refueling and Outage Activities (71111.20)
a. Inspection Scope
The inspectors observed the licensee's performance during Refueling Outage B1R14 beginning September 10, 2006. As of September 30, 2006, the licensee has not
finished all the outage activities. Therefore the inspection sample was not competed for
this report.
The inspectors evaluated the licensee's conduct of refueling outage activities to assess the licensee's control of plant configuration and management of shutdown risk. The
inspectors reviewed configuration management to verify that the licensee maintained
defense-in-depth commensurate with the shutdown risk plan; reviewed major outage
work activities to ensure that correct system lineups were maintained for key mitigating
systems; and observed refueling activities to verify that fuel handling operations were
performed in accordance with the TS, TRM, UFSAR and approved procedures. The
inspectors interviewed operations, engineering, work control, radiological protection, and
maintenance department personnel during their inspection activities. The inspectors 13 also attended outage-related status and pre-job briefings as well as Radiation Protection ALARA [As Low As Reasonably Achievable] briefings. Other major outage activities
evaluated included evaluating the licensee's control of:*containment penetrations in accordance with the TS;*structures, systems or components (SSCs) which could cause unexpected reactivity changes;*flow paths, configurations, and alternate means for reactor coolant system inventory addition;*SSCs which could cause a loss of inventory;
- RCS pressure, level, and temperature instrumentation;
- spent fuel pool cooling during and after core offload;
- switchyard activities and the configuration of electrical power systems in accordance with the TS and shutdown risk plan; and*SSCs required for decay heat removal.
The inspectors observed portions of the plant cooldown, including the transition to shutdown cooling, to verify that the licensee controlled the plant cooldown in accordance
with the TS. In addition, the inspectors completed numerous visual inspections inside
the Unit 1 containment. This included a tour of the Unit 1 containment at Mode 3 during
the cooldown at the beginning of B1R14 so that the inspectors could assess the initial
material condition of equipment inside containment immediately following the operating
cycle. During the visual inspections the inspectors focused on the material condition of
the equipment and particularly on any indication of boric acid.
In addition, the inspectors evaluated portions of the restart preparation activities to verify that requirements of the TS and administrative procedure requirements were met prior to
changing operational modes or plant configurations. Major restart preparation
inspection activities performed included:*verification that core reload was completed in accordance with the core loading plan for Byron Unit 1 Cycle 14;*evaluation of foreign material exclusion control practices during significant work activities;*verification that correct system lineups were maintained for key mitigatingsystems; and*inspection of the containment building to assess material condition and search for loose debris, which if present, could be transported to the containment
recirculation sumps and cause restriction of flow to the emergency core cooling
system pump suctions during loss-of-coolant accident conditions.
The documents reviewed during this inspection are listed in the Attachment to this report.
b. Findings
No findings of significance were identified.
141R22Surveillance Testing (71111.22)
a. Inspection Scope
The inspectors witnessed selected surveillance tests and/or reviewed test data to determine that the equipment tested using the surveillance procedures met the TS, the
TRM, the UFSAR and licensee procedural requirements. The inspectors also reviewed
applicable design documents including plant drawings, to verify that the surveillance
tests demonstrated that the equipment was capable of performing its intended safety
functions. The activities were selected based on their importance in ensuring mitigating
systems capability and barrier integrity.
These activities represented six routine samples. The following surveillance tests were selected:*Unit 2 Train A Emergency Diesel Generator Monthly Operability Run;*Unit 1 Reactor Containment Fan Cooler Monthly Surveillance;
- Unit 2 Train B Solid State Protection System Bi-Monthly Surveillance;
- Unit 1 Simultaneous Start of Both Auxiliary Feedwater Pumps;
- Unit 1 Train B Diesel Generator Safety Injection Sequencer Test; and
- Unit 1 Division 11 A Train 125V Battery Bank Service Test.
Additionally the inspectors used the documents listed in the attachment to this report to determine that the testing met the frequency requirements; that the tests were
conducted in accordance with procedures, that the test acceptance criteria were met;
and that the results of the tests were properly reviewed and recorded. The inspectors
verified that the individuals performing the tests were qualified to perform the test in
accordance with the licensee's requirements, and that the test equipment used during
the test were calibrated within the specified periodicity. In addition, the inspectors
interviewed operations, maintenance, and engineering department personnel regarding
the tests and test results. The documents reviewed during this inspection are listed in the Attachment to this report.
b. Findings
No findings of significance were identified.1EP6Drill Evaluation (71114.06)
a. Inspection Scope
On August 22, 2006, the inspectors complete one inspection sample by observing an Out of the Box Operator Requalification training that had emergency preparedness
exercise aspects. The inspectors assessed the licensee's exercise performance and
looked for weaknesses in the risk significance areas of emergency classification, notification and protective action development. The inspectors observed the licensee's
performance from the simulator control room. The inspectors compared issues noted 15 during their observations to those identified during the licensee's critique. Additionally, the inspectors verified that items identified during the licensee's critique were
appropriately entered into their corrective action program.
The documents reviewed during this inspection are listed in the Attachment to this report.
b. Findings
No findings of significance were identified.2.RADIATION SAFETY
===Cornerstone: Occupational Radiation Safety2OS1Access Control to Radiologically Significant Areas (IP 71121.01).1Plant Walkdowns and Radiation Work Permit Reviews
a. Inspection Scope
=
The inspectors reviewed licensee controls and surveys in the following three radiologically significant work areas within radiation areas, high radiation areas and
airborne radioactivity areas in the plant and reviewed work packages which included
associated licensee controls and surveys of these areas to determine if radiological
controls including surveys, postings and barricades were acceptable: *Emergency Core Cooling System (ECCS) Sump Modification;*Pressurizer Weld Overlay; and
- Reactor Disassembly.
This review represented one inspection sample.
The inspectors reviewed the radiation work permits (RWPs) and work packages used to access these three areas and other high radiation work areas to identify the work control
instructions and control barriers that had been specified. Electronic dosimeter alarm set
points for both integrated dose and dose rate were evaluated for conformity with survey
indications and plant policy. Workers were interviewed to verify that they were aware of
the actions required when their electronic dosimeters noticeably malfunctioned or
alarmed. This review represented one inspection sample.
The inspectors walked down and surveyed (using an NRC survey meter) these three areas to verify that the prescribed RWP, procedure, and engineering controls were in
place; that licensee surveys and postings were complete and accurate; and that air
samplers were properly located. This review represented one inspection sample.
The inspectors reviewed RWPs for potential airborne radioactivity areas to verify barrier integrity and engineering controls performance (e.g., HEPA ventilation system
operation) and to determine if there was a potential for individual worker internal 16 exposures of greater than 50 millirem committed effective dose equivalent. There were no areas where there was a potential for individual worker internal exposures of greater
than 50 millirem committed effective dose equivalent. Work areas having a history of, or
the potential for, airborne transuranics were evaluated to verify that the licensee had
considered the potential for transuranic isotopes and provided appropriate worker
protection. There where no areas having a history of, or the potential for, airborne
transuranics. This review represented one inspection sample.
The adequacy of the licensee's internal dose assessment process for any actual internal exposures greater than 50 millirem committed effective dose equivalent was assessed.
There were no internal exposures greater than 50 millirem committed effective dose
equivalent. This review represented one inspection sample.
b. Findings
Introduction
- A finding of very low safety significance and two associated Non-Cited Violations of NRC requirements were identified for the failure to post and control access
to a high radiation area.
Description
- A walkdown of the facility was conducted by the NRC inspectors and a member of the licensee's staff during the afternoon of September 11, 2006. This
walkdown identified that an opening of approximately 3'x4' in size that led to a pipe
chase next to the Unit 1 Filter Valve Aisle located on the 383' elevation of the Auxiliary
Building. This opening was created when a portion of a block shield wall was removed
to support a specific job evolution in the Unit 1 Filter Valve Aisle. The inspectors
questioned the licensee staff as to the systems that lie within the pipe chase that was
rendered accessible by removing the blocks. Based upon the answer provided and the
upcoming scheduled plant evolution of forced oxidation, the inspectors questioned the
characterization of the pipe chase and the adequacy of the posting and controls for the
current conditions or the expected conditions over the next few hours.
The forced oxidation process is performed to reduce or remove radioactive source term from the primary coolant system and, therefore, to lower the personnel dose that is
accumulated during the refueling outage. The process introduces a chemical to the
reactor coolant system which loosens material that has plated out inside the system.
This material is removed from the system via plant demineralizers and through filtration, usually within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. The licensee implemented controls for areas that had been
defined based upon previous plant experiences. The block shield wall was intact, different than current configuration, during previous evolutions of forced oxidation.
The licensee completed the survey of this area at 0100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br /> on September 13, 2006, approximately 26 hours3.009259e-4 days <br />0.00722 hours <br />4.298942e-5 weeks <br />9.893e-6 months <br /> after initiating the forced oxidation process. That survey
identified dose rates in excess of 100 mR/hour at the plane of the opening. These
conditions met the definition as a High Radiation Area, but the area was not posted or
controlled as a High Radiation Area.
Analysis:
The failure to post and control access to High Radiation Areas represents a performance deficiency as defined in NRC Inspection Manual Chapter (IMC) 0612, "Power Reactor Inspection Reports," Appendix B, "Issue Screening." The inspectors 17 determined that the issue was associated with the Program/Process attribute of the Occupational Radiation Safety Cornerstone and affected the cornerstone objective to
ensure the adequate protection of the worker health and safety from exposure to
radiation from radioactive material during routine civilian nuclear reactor operation.
Therefore, the issue was more than minor and represented a finding which was
evaluated using the Significance Determination Process (SDP).
Since the finding involved the ability to protect workers from exposure to radiation, the inspectors utilized IMC 0609, Appendix C, "Occupational Radiation Safety SDP," to
assess its significance. The inspectors determined that the finding did not concern
unintended collective dose resulting from a deficiency in the ALARA planning or work
control or exposure control. The inspectors also determined that the finding did not
involve an overexposure or the substant ial potential for an overexposure. The inspectors determined that the finding did not compromise the licensee's ability to
assess dose. Consequently, the inspectors concluded that the SDP assessment for this
finding was of very low safety significance (Green).
As described above, the removal of the ~ 3'x4' block wall was authorized to support a work activity. However, the evaluation that provided this authorization was not sufficient
to provide limits, controls, or compensatory actions for subsequent plant evolutions.
Consequently, this deficiency has a cross cutting aspect for Human Performance.
Specifically, the licensee did not use a systematic decision making process and did not
obtain interdisciplinary input on a risk-significant decision.
Enforcement
- 10 CFR 20.1902 requires the licensee to post each high radiation area with a conspicuous sign or signs bearing the radiation symbol and the words "CAUTION, HIGH RADIATION AREA" or "DANGER, HIGH RADIATION AREA. Additionally, 10
CFR 20.1601 specifies the requirements for control of access to high radiation areas.
As provided in Technical Specification 5.7.1, the licensee is authorized to implement
alternate controls to those stated in 10 CFR 20.1601 for areas that do not exceed 1000
millirem per hour.
Contrary to the above, as of 0100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br /> on September 13, 2006, the entrance to the Unit 1 Filter Valve Aisle located on the 383' elevation of the Auxiliary Building, a high
radiation area with a radiation dose rate of approximately 135 millirem in one hour at
plane of the penetration, was not posted or controlled by any of the methods described
in 10 CFR 20.1902, 10 CFR 20.1601, or Technical Specification 5.7.1.
Corrective actions taken by the licensee included making the pipe chase inaccessible by bolting a plate over the opening and placing information postings over the bolted plate.
In addition, the licensee revised the posting and controls within the Unit 1 Filter Valve
Aisle to that of a high radiation area. Since the licensee documented this issue in its
corrective action program (IR 531013) and because the violations are of very low safety
significance, they are being treated as Non-Cited Violations (NCV 05000454/2006004-02; 05000455/2006004-02).
.2 Problem Identification and Resolution
a. Inspection Scope
18 The inspectors reviewed three corrective action reports related to access controls and high radiation area radiological incidents. Staff members were interviewed and
corrective action documents were reviewed to verify that follow-up activities were being
conducted in an effective and timely manner commensurate with their importance to
safety and risk based on the following:*initial problem identification, characterization, and tracking;*disposition of operability/reportability issues;
- evaluation of safety significance/risk and priority for resolution;
- identification of repetitive problems;
- identification of contributing causes;
- identification and implementation of effective corrective actions;
- resolution of Non-Cited Violations (NCVs) tracked in the corrective action system; and*implementation/consideration of risk significant operational experience feedback.
This review represented one inspection sample.
b. Findings
No findings of significance were identified.
.3 Job-In-Progress Reviews
a. Inspection Scope
The inspectors observed the following three jobs that were being performed in radiation areas, airborne radioactivity areas, or high radiation areas for observation of work
activities that presented the greatest radiological risk to workers: *ECCS Sump Modification;*Pressurizer Weld Overlay; and
- Reactor Disassembly.
The inspectors reviewed radiological job requirements for these three activities including RWP requirements and work procedure requirements, and attended As-Low-As-Is-
Reasonably-Achievable (ALARA) job briefings. This review represented one inspection sample. Job performance was observed with respect to these requirements to verify that radiological conditions in the work area were adequately communicated to workers
through pre-job briefings and postings. The inspectors also verified the adequacy of
radiological controls including required radiation, contamination, and airborne surveys
for system breaches; radiation protection job coverage which included audio and visual
surveillance for remote job coverage; and contamination controls. This review
represented one inspection sample.
b. Findings
19 No findings of significance were identified.
.4 Radiation Worker Performance
a. Inspection Scope
During job performance observations, the inspectors evaluated radiation worker performance with respect to stated radiation protection work requirements and evaluated
whether workers were aware of the significant radiological conditions in their workplace, the RWP controls and limits in place, and that their performance had accounted for the
level of radiological hazards present. This review represented one inspection sample.
The inspectors reviewed radiological problem reports which found that the cause of the event was due to radiation worker errors to determine if there was an observable pattern
traceable to a similar cause and to determine if this perspective matched the corrective
action approach taken by the licensee to resolve the reported problems. These
problems, along with planned and taken corrective actions were discussed with the
Radiation Protection Manager. This review represented one inspection sample.
b. Findings
No findings of significance were identified..5Radiation Protection Technician (RPT) Proficiency
a. Inspection Scope
During job performance observations, the inspectors evaluated RPT performance with respect to radiation protection work requirements and evaluated whether they were
aware of the radiological conditions in their workplace, the RWP controls and limits in
place, and if their performance was consistent with their training and qualifications with
respect to the radiological hazards and work activities. This review represented one
inspection sample.
The inspectors reviewed radiological problem reports which, found that the cause of the event was radiation protection technician error, to determine if there was an observable
pattern traceable to a similar cause and to determine if this perspective matched the
corrective action approach taken by the licensee to resolve the reported problems. This
review represented one inspection sample.
b. Findings
No findings of significance were identified.2OS2As-Low-As-Is-Reasonably-Achievable Planning and Controls (ALARA) (IP 71121.02).1
Inspection Planning
a. Inspection Scope
20 The inspectors reviewed plant collective exposure history, current exposure trends, ongoing and planned activities in order to assess current performance and exposure
challenges. This included determining the plant's current 3-year rolling average for
collective exposure in order to help establish resource allocations and to provide a
perspective of significance for any resulting inspection finding assessment. This review
represented one inspection sample.
The inspectors reviewed the outage work scheduled during the inspection period and associated work activity exposure estimates fo r the following three work activities which were likely to result in the highest personnel collective exposures: *Emergency Core Cooling System (ECCS) Sump Modification;*Pressurizer Weld Overlay; and
- Reactor Disassembly.
This review represented one inspection sample.
The inspectors reviewed site specific trends in collective exposures and source-term measurements. The inspectors reviewed procedures associated with maintaining
occupational exposures ALARA and processes used to estimate and track work activity
specific exposures. This review represented two inspection samples.
b. Findings
No findings of significance were identified..2Radiological Work Planning
a. Inspection Scope
The inspectors evaluated the licensee's list of planned work activities for Unit 1 Refueling Outage 14 ranked by estimated exposure that were in progress and reviewed
the following three work activities of exposure significance: *Emergency Core Cooling System (ECCS) Sump Modification;*Pressurizer Weld Overlay; and
- Reactor Disassembly.
This review represented one inspection sample.
For these three activities, the inspectors re viewed the ALARA work activity evaluations, exposure estimates, and exposure mitigation requirements in order to verify that the
licensee had established procedures and engineering and work controls that were based
on sound radiation protection principles in order to achieve occupational exposures that
were ALARA. This also involved determining if the licensee had reasonably grouped the
radiological work into work activities, based on historical precedence, industry norms, and/or special circumstances. This review represented one inspection sample.
The inspectors compared the results achieved, including dose rate reductions and 21 person-rem used, with the intended dose established in the licensee's ALARA planning for these three work activities. Reasons for inconsistencies between intended and
actual work activity doses were review ed. This review represented one inspectionsample.
b. Findings
No findings of significance were identified..3Verification of Dose Estimates and Exposure Tracking Systems
a. Inspection Scope
The licensee's process for adjusting exposure estimates or re-planning work, when unexpected changes in scope, emergent work or higher than anticipated radiation levels
were encountered, was evaluated. This included determining whether adjustments to
estimated exposure (intended dose) were based on sound radiation protection and
ALARA principles and not adjusted to account for failures to control the work. The
frequency of these adjustments was reviewed to evaluate the adequacy of the original
ALARA planning process. This review represented one inspection sample.
b. Findings
No findings of significance were identified..4Job Site Inspections and ALARA Control
a. Inspection Scope
The inspectors observed the following three jobs that were being performed in radiation areas, airborne radioactivity areas, or high radiation areas for observation of work
activities that presented the greatest radiological risk to workers.*Emergency Core Cooling System (ECCS) Sump Modification;*Pressurizer Weld Overlay; and
- Reactor Disassembly.
The licensee's use of engineering controls to achieve dose reductions was evaluated to verify that procedures and controls were consistent with the licensee's ALARA reviews, that sufficient shielding of radiation sources was provided, and that the dose expended
to install/remove the shielding did not exceed the dose reduction benefits afforded by the
shielding. This review represented one inspection sample.
b. Findings
No findings of significance were identified.
.5 Radiation Worker Performance
a. Inspection Scope
Radiation worker and RPT performance was observed during work activities being performed in radiation areas, airborne radioactivity areas, and high radiation areas that
presented the greatest radiological risk to workers. The inspectors evaluated whether
workers demonstrated the ALARA philosophy in practice by being familiar with the work
activity scope and tools to be used, by utilizing ALARA low dose waiting areas and that
work activity controls were being complied with. Also, radiation worker training and skill
levels were reviewed to determine if they were sufficient relative to the radiological
hazards and the work involved. This review represented one inspection sample.
b. Findings
No findings of significance were identified.2OS3Radiation Monitoring Instrumentation and Protective Equipment (71121.03).1
Inspection Planning
a. Inspection Scope
The inspectors reviewed the Byron Station Updated Final Safety Analysis Report (UFSAR) to identify applicable radiation monitors associated with measuring transient
high and very high radiation areas including those used in remote emergency
assessment. The inspectors identified the types of portable radiation detection
instrumentation used for job coverage of high radiation area work including instruments
used for underwater surveys, fixed area radiat ion monitors used to provide radiological information in various plant areas, and continuous air monitors used to assess airborne
radiological conditions and work areas with the potential for workers to receive a
50 millirem or greater committed effective dose equivalent (CEDE). Contamination monitors, whole body counters, and those radiation detection instruments utilized for the
release of personnel and equipment from the radiologically controlled area (RCA) were
also identified.
These reviews represented two inspection samples.
b. Findings
No findings of significance were identified..2Walkdowns of Radiation Monitoring Instrumentation
a. Inspection Scope
The inspectors conducted walkdowns of selected area radiation monitors (ARMs)in the Unit 1 and 2 Auxiliary Buildings to verify that they were located as described in
the UFSAR and were adequately positioned relative to the potential source(s) of
radiation they were intended to monitor. Walkdowns were also conducted of those
areas where portable survey instruments were calibrated/repaired and maintained for 23 radiation protection (RP) staff use to determine if those instruments designated "ready for use" were sufficient in number to support the radiation protection program, had
current calibration stickers, were operable, and were in adequate physical condition.
Additionally, the inspectors observed the licensee's instrument calibration units and the
radiation sources used for instrument checks to assess their material condition and
discussed their use with RP staff to determine if they were used appropriately. Licensee
personnel demonstrated the methods for performing source checks of portable survey
instruments and for source checking personnel contamination and portal monitors used
at the egress to the RCA.
These reviews represented one inspection sample.
b. Findings
No findings of significance were identified.
.3 Calibration and Testing of Radiation Monitoring Instrumentation
a. Inspection Scope
Portable survey instrument calibrations were performed at an offsite Exelon facility.
Licensee personnel were observed performing source checks of selected instruments.
This included observing detector evaluation with check sources to determine if station
requirements were met. The inspectors reviewed records of calibration, operability, and
alarm setpoints of selected instruments and personnel monitoring devices. This review
included, but was not limited to the following:*Certificate of Calibration for Eberline Radiation Detection Device Model ASP-1/AC3-7, Serial No. 652/724197;*Certificate of Calibration for Eberline Radiation Detection Device Model E-530, Serial No. 1337; *Certificate of Calibration for Eberline Radiation Detection Device Model RM-14, Serial Nos. 7382 and 7528;*Calibration of Nuclear Enterprises Small Articles Monitor (SAM), Serial No. 478;
- Units 1 and 2 High Range Containment Radiation Monitors; and
- Auxiliary Building Vent Stack Wide Range Gas Radiation Monitor.
The inspectors evaluated those actions that would be taken when, during calibration or source checks, an instrument was found to be out of calibration by more than
50 percent. Those actions included an investigation of the instrument's previous usages
and the possible consequences of that usage since the last calibration or source check.
The inspectors also reviewed the licensee's 10 CFR Part 61 source term analyses to
determine if the calibration sources used were representative of the plant source term.
This review represented one sample.
b. Findings
No findings of significance were identified.
24.4Problem Identification and Resolution
a. Inspection Scope
The inspectors reviewed the licensee's self-assessments, audits, and condition reports that involved personnel contamination monitor alarms due to personnel internal
exposures to determine if identified problems were entered into the corrective action
program for resolution. There were no internal exposure occurrences greater than
50 millirem committed effective dose equivalent that were evaluated during the
inspection. However, the licensee's process for investigating this type of occurrence
was reviewed to determine if the affected personnel would be properly monitored
utilizing the appropriate equipment and if the data would be analyzed and internal
exposures properly assessed in accordance with licensee procedures. This review
represented one sample.
The inspectors reviewed corrective action program reports related to exposure of significant radiological incidents that involved radiation monitoring instrument
deficiencies since the last inspection in this area. Staff members were interviewed and
corrective action documents were reviewed to determine if follow-up activities were
being conducted in an effective and timely m anner commensurate with its importance to safety and risk based on the following:*Initial problem identification, characterization, and tracking;*Disposition of operability/reportability issues;
- Evaluation of safety significance/risk and priority for resolution;
- Identification of repetitive problems;
- Identification of contributing causes;
- Identification and implementation of effective corrective actions;
- Resolution of Non-Cited Violations tracked in the corrective action system; and
- Implementation/consideration of risk significant operational experience feedback.
This review represented one sample.
The inspectors evaluated the licensee's self-assessment activities to determine if they would identify and address repetitive deficiencies or significant individual deficiencies
observed in problem identification and resolution. This review represented one sample.
b. Findings
No findings of significance were identified.5Radiation Protection Technician Instrument Use
a. Inspection Scope
The inspectors determined if the calibration expiration and source response check data records on radiation detection instruments staged for use were current and observed
radiation protection technicians for appropriate instrument selection and self-verification
of instrument operability prior to use. This review represented one sample.
b. Findings
No findings of significance were identified..6Self-Contained Breathing Apparatus (SCBA) Maintenance/Inspection and User Training
a. Inspection Scope
The inspectors reviewed the status, maintenance and surveillance records of selected self-contained breathing apparatuses staged and ready for use in the plant and
assessed the licensee's capability for refilling and transporting self-contained breathing
apparatus air bottles to and from the control room during emergency conditions. The
inspectors determined whether control room operators and other emergency response
and radiation protection personnel were trained and qualified in the use of self-contained
breathing apparatuses including personal bottle change-out. The inspectors also
reviewed the training and qualification records for selected individuals on each control
room shift crew and selected individuals from each designated department that were
currently assigned emergency duties, including onsite search and rescue. This review
represented one sample.
The inspectors reviewed the self-contained breathing apparatus manufacturer's maintenance training certifications for licensee personnel qualified to perform self-
contained breathing apparatus maintenance on vital components (regulator and low
pressure alarm). The inspectors reviewed maintenance records for several self-
contained breathing apparatuses designated as "ready for service." The inspectors
verified that maintenance was performed by qualified personnel over the past five years.
The inspectors also determined if the required, periodic air cylinder hydrostatic testing
was current and documented. The inspectors also evaluated if the licensee's
maintenance procedures were consistent with the self-contained breathing apparatus
manufacturer's maintenance manuals. This review represented one sample.
b. Findings
No findings of significance were identified.
Cornerstone: Public Radiation Safety
2PS1Radioactive Gaseous and Liquid Effluent Treatment and Monitoring Systems (71122.01).1Integrity of the Circulating Water Blowdown Line
a. Inspection Scope
The inspectors reviewed the licensee's evaluation associated with Unresolved Item (URI) 050000454/2006002-02; 050000455/2006002-02 regarding the licensee's lack of
a circulating water blowdown line pipe integrity verification. Industry experience had
shown that the failure of circulating water blow-down line vacuum breakers resulted in
the release of contaminated water into the offsite environment resulting in groundwater
contamination. On February 2, 2006, the licensee could not demonstrate the integrity of 26 circulating water blowdown line vacuum breakers. Leakage of water from the blow-down line could result in the release of radioactive material into the environment via a release
path that was undefined in the ODCM and had no offsite dose estimates, and as
documented as an URI.
The inspectors reviewed the licensee's radiological assessment of leaks from the circulating water (CW) blowdown line that was identified in February 2006. The
inspectors reviewed historical records to evaluate the licensee's response to the leaks, including radiological surveys, dose assessments, and mitigative actions. The
inspectors' evaluation was performed to determine if the licensee adequately
implemented the requirements contained in 10 CFR Part 20 and the licensee's Technical
Specifications. The inspectors also reviewed:*Radiation protection surveys for affected areas;*Maintenance work orders for selected vacuum breaker valves associated with the releases;*Identification of potential pathways based upon release location;
- Reports contained in the licensee's corrective action program for these events;
- Parameters and results of licensee's groundwater characterization study;
- Files that contain environmental contamination events; and
- Select annual effluent release reports.
Additionally, the inspector's evaluated the licensee's corrective actions that included:
- Sealing the vacuum breaker valve vaults (via grout and a waterproofing application);*Performing inspection and maintenance on the vacuum breaker valves;
- Installation of additional groundwater monitoring wells;
- Visual observations of each vacuum breaker valve vault during radioactive releases to identify leakage (compensatory action); and *Installation of an automated leak detection system.
b. Findings
Introduction
- A finding of very low safety significance and an associated non-cited violation of NRC requirements were identified for the failure to survey water for
radioactive materials before releasing to the ground.
Description
- The licensee began formally inspecting vacuum breaker valves in 1999 as result of a failure of similar vacuum breaker valves at the Braidwood facility. The
licensee attributed the presence of small amounts of water found in the vacuum breaker
vaults to be ground water that infiltrated the through a drain in the vault or from rain
water that seeped under the vault cover. On July 7, 2005, the vault containing valve
0CW276 (vault No. 6) was filled with water, and there were other indications that the
source was not ground water infiltration. Despite these indications, the vault was
emptied by pumping the water to ground. The licensee did not assess the source of the
water nor did the licensee perform a radiological survey prior to pumping the water to the
ground. The licensee recognized the potential for this water to contain radioactive
material from the liquid radioactive waste program when the failed valve was entered 27 into the corrective action program. Subsequently, the licensee performed an investigation that included sampling the soil around the vault for the presence of
radionuclides. The investigation was limited to analyzing the soil surrounding the
affected vault, as the area did not have free standing water. This analysis was
completed within two weeks from the time the condition was identified and determined
that the area was free from gamma emitting radionuclides.
During an NRC baseline inspection in the area of Radioactive Gaseous and Liquid Effluent Treatment and Monitoring Systems in February 2006, the inspectors questioned
the licensee's evaluation of water that exist ed in the vacuum breaker valve vaults and the lack of radiological measurements of that water. In response to these questions, the
licensee then identified standing water in 5 of the 6 vaults with tritium concentrations
from 1,000 picocuries per liter to 80,000 picocuries per liter. Based on these sample
results, the licensee installed ground water monitoring wells near the six vacuum breaker
valve vaults along the station's discharge pipe to allow further sampling for tritium. Wells
beside four of the six vaults showed no detectable levels of tritium. Test wells beside the
other two showed low levels of tritium. One showed a concentration of about
3800 picocuries per liter, the other about 450 picocuries per liter. The licensee's
radiological environmental monitoring pr ogram (Rev. 2, 2002) included waterborne sampling/analyses from wells located 0.7 mile s, 1.0 miles, and 1.8 miles from the plant site and in the general area of the blowdown line. The licensee's results from these
wells as well as the 6 newly installed wells did not identified any detectable tritium
migration beyond the licensee's property.
Although the licensee recognized in July 2005 that water was apparently leaking from the valve and recognized the potential that leakage from a blowdown line vacuum
breaker could represent an unevaluated condition, the licensee did not take actions
necessary to evaluate the radiological hazards associated with leakage. Furthermore, the corrective action evaluation performed by the licensee in August 2005 did not
address or modify plant procedures or work order packages for inspection of vacuum
breakers to prevent further pumping water from the vaults to ground with sampling.
Analysis:
The failure to evaluate the potential radiological hazard associated with the leakage of water from the vacuum breaker valves and the subsequent discharge of that
water to the ground represents a performance deficiency as defined in NRC Inspection
Manual Chapter (IMC) 0612, "Power Reactor Inspection Reports," Appendix B, "Issue
Screening." The inspectors determined that the issue was associated with the
Program/Process attribute of the Public Radiation Safety Cornerstone and affected the
cornerstone objective to ensure adequate protection of public health and safety from
exposure to radioactive materials released into the public domain as a result of routine
civilian nuclear reactor operation. Therefore, the issue was more than minor and
represented a finding which was evaluated using the Significance Determination
Process (SDP).
Since the finding involved the ability to assess dose from radioactive effluents and maintain radiation doses to a member of the public within Appendix I design objectives, the inspectors utilized IMC 0609, Appendix D, "Public Radiation Safety SDP," to assess
its significance. The inspectors determined that the finding did not involve Radioactive
Material Control. Since the release did not migrate off the licensee's property, the 28 inspectors utilized the Effluent Release Program branch of the SDP. Although the licensee analyzed the surrounding soil for the release of gamma emitting radionuclides, tritium was not included in the analysis because the liquid content was no longer
available after pumping the vault. Tritium is the most predominant radionuclide in a
typical liquid radioactive waste release. Therefore, this limitation impaired the licensee's
ability to assess dose. The licensee's current sampling and evaluation did not indicate
any measurable release of radioactive material beyond the licensee's property. These
results indicated that the assessment of off site dose was not warranted; therefore, the
licensee did not fail to assess dose to the public. Consequently, the inspectors
concluded that the SDP assessment for this finding was of very low safety significance (Green).As described above, the licensee's August 2005 evaluation was limited to the water that was pumped out of vault No. 6 on July 7, 2005. The inspectors identified that the
evaluation did not review or change the practice of pumping water directly from the vault at any other vacuum breaker. Consequently, this deficiency has a cross cutting aspect
for Problem Identification and Resolution. Specifically, the corrective action evaluation
performed by the licensee in August 2005 did not address or modify plant procedures or work order packages for inspection of vacuum breakers to prevent pumping water from
the vaults to ground with sampling.
Enforcement
- 10 CFR 20.1501 requires that each licensee make or cause to be made surveys that may be necessary for the licensee to comply with the regulations in
10 CFR Part 20 and that are reasonable under the circumstances to evaluate the extent
of radiation levels, concentrations or quantities of radioactive materials, and the potential
radiological hazards that could be present.
Pursuant to 10 CFR 20.1003, survey means an evaluation of the radiological conditions and potential hazards incident to the production, use, transfer, release, disposal, or
presence of radioactive material or other sources of radiation.
Contrary to the above, as of February 8, 2006, the licensee did not make adequate surveys to assure compliance with 10 CFR 20.1301, which limits radiation exposure to a
member of the public to 0.1 rem. Specifically, the conditions found at valve 0CW276 (vault No. 6) on July 7, 2005, were outside the parameters of the licensee's original
assessment, and the licensee did not evaluate the change of conditions for the potential
radiological hazards. A review of historical records indicated other occurrences of
pumping water from the vacuum breaker vaults to the ground without performing a survey.Corrective actions taken by the licensee for this finding included performing surveys of the soil surrounding the vacuum breaker vault, establishing additional groundwater
monitoring wells, sealing the vacuum breaker vaults, and installing an automated leak
detection system. Since the licensee documented this issue in its corrective action
program (AR 350931 and subsequent Apparent Cause Evaluation No. 478372) and
because the violation is of very low safety significance, it is being treated as a Non-Cited
Violation (NCV 05000454/2006004-03; 05000455/2006004-03). The associated URI is
closed.
292PS2Radioactive Material Processing and Transportation (71122.02).1Radioactive Waste System
Inspection Planning
a. Inspection Scope
The inspectors reviewed the liquid and solid radioactive waste system description in the UFSAR for information on the types and amounts of radioactive waste (radwaste)
generated and disposed. The inspectors reviewed the scope of the licensee's audit
program with regard to radioactive material processing and transportation programs to
verify that it met the requirements of 10 CFR 20.1101©). This review represented one sample.
b. Findings
No findings of significance were identified..2Walkdown of Radioactive Waste Systems
a. Inspection Scope
The inspectors reviewed the liquid and solid radioactive waste system description in the UFSAR and the most recent information regarding the types and amounts of radioactive
waste generated and disposed. The inspectors performed walkdowns of the liquid and
solid radwaste processing systems to ve rify that the systems agreed with the descriptions in the Updated Safety Analysis Report and the Process Control Program
and to assess the material condition and operability of the systems. The inspectors
reviewed changes to the waste processing system to verify the changes were reviewed
and documented in accordance with 10 CFR 50.59 and to assess the impact of the
changes on radiation dose to members of the public.
The inspectors reviewed the current processes for transferring waste resins into transportation containers to determine if appropriate waste stream mixing and/or
sampling procedures were utilized. The inspectors also reviewed the methodologies for
waste concentration averaging to determine if representative samples of the waste
product were provided for the purposes of waste classification in accordance with
10 CFR 61.55. During this inspection, the licensee was not conducting waste
processing. This review represented one sample.
b. Findings
No findings of significance were identified..3Waste Characterization and Classification
a. Inspection Scope
The inspectors reviewed the licensee's radiochemical sample analysis results for each of the licensee's waste streams, including dry active waste, resins, and filters. The 30 inspectors also reviewed the licensee's use of scaling factors to quantify difficult-to-measure radionuclides (e.g., pure alpha or beta emitting radionuclides). The reviews
were conducted to verify that the licensee's program assured compliance with
10 CFR 61.55 and 10 CFR 61.56, as required by Appendix G of 10 CFR Part 20. The
inspectors also reviewed the licensee's waste characterization and classification
program to ensure that the waste stream composition data accounted for changing
operational parameters and thus remained valid between the annual sample analysis
updates. This review represented one sample.
b. Findings
No findings of significance were identified..4Shipment Preparation
a. Inspection Scope
The inspectors reviewed shipment packaging, surveying, labeling, marking, placarding, vehicle checks, emergency instructions, disposal manifest, shipping papers provided to
the driver, and licensee verification of shipment readiness for a dry active waste
shipment. The inspectors verified that the receiving licensee was authorized to receive
the shipment packages. The inspectors reviewed the licensee's procedures for loading
and closure. The inspectors observed radiation worker practices to verify that the
workers had adequate skills to accomplish each task and to determine if the shippers
were knowledgeable of the shipping regulations and whether shipping personnel
demonstrated adequate skills to accomplish the package preparation requirements for
public transport with respect to NRC Bulletin 79-19 and 49 CFR Part 172 Subpart H.
The inspectors reviewed the training provided to personnel responsible for the conduct
of radioactive waste processing and radioactive shipment preparation activities. The
review was conducted to verify that the licensee's training program provided training
consistent with NRC and Department of Transportation (DOT) requirements. This
review represented one sample.
b. Findings
No findings of significance were identified..5Shipping Records
a. Inspection Scope
The inspectors reviewed ten non-excepted package shipment manifests completed in years 2005 and 2006 to verify compliance with USNRC and Department of
Transportation requirements (i.e., 10 CFR Parts 20 and 71 and 49 CFR Parts 172
and 173). The inspector reviewed current package preparation or shipping underway
during the inspection. This review represented one sample.
b. Findings
31 No findings of significance were identified..6Identification and Resolution of Problems
a. Inspection Scope
The inspectors reviewed condition reports, audits, and self-assessments that addressed radioactive waste and radioactive materials shipping program deficiencies since the last
inspection, to verify that the licensee had effectively implemented the corrective action
program and that problems were identified, characterized, prioritized and corrected. The
inspectors also verified that the licensee's self-assessment program was capable of
identifying repetitive deficiencies or significant individual deficiencies in problem
identification and resolution.
The inspectors also reviewed corrective action reports from the radioactive material and shipping programs since the previous inspection, interviewed staff and reviewed
documents to determine if the following activities were being conducted in an effective
and timely manner commensurate with their importance to safety and risk:*Initial problem identification, characterization, and tracking;*Disposition of operability/reportability issues;
- Evaluation of safety significance/risk and priority for resolution;
- Identification of repetitive problems;
- Identification of contributing causes;
- Identification and implementation of effective corrective actions;
- Resolution of non-cited violations (NCVs) tracked in corrective action system(s);
and*Implementation/consideration of risk significant operational experience feedback.
This review represented one sample.
b. Findings
No findings of significance were identified.2PS3Radiological Environmental Monitoring Program (REMP) and Radioactive Material Control Program (71122.03).1Reviews of Radiological Environmental Monitoring Reports, Data and Quality Control
a. Inspection Scope
The NRC performed a number of confirmatory measurements of water samples to evaluate the licensee's proficiency in collecting and in analyzing water samples for
tritium and other radioactive isotopes. The samples were collected independently by the
inspectors and/or by licensee personnel and sent to the NRC's contract laboratory for
the analysis of tritium. The NRC and licensee obtained these samples from surface
water and groundwater sampling points identified in the licensee's Radiological
Environmental Monitoring Program and from onsite and offsite groundwater monitoring 32 wells. In particular, samples were obtained as part of the licensee's environmental study of tritium and potential groundwater contamination (ADAMS ML062750384) and as part
of an evaluation of leakage from the circulating water blowdown line that is documented
in Section 2PS1 of this report. While tritium was the primary radionuclide of concern, selected samples were also analyzed for gamma emitting radionuclides and for
strontium. The inspectors performed these reviews to assess the licensee's analytical
detection capabilities for radio-analysis of environmental samples and its ability to
accurately quantify radionuclides to an acceptable level of sensitivity. The criteria used
to compare the sample results is provided in Attachment 2, and the results of the
comparisons between the NRC and licensee results is provided in Attachment 3.
The inspectors considered the following activities in evaluating the cause of any comparisons that did not result in an agreement:*re-analysis by licensee or NRC's contract laboratory;*review of licensee's interlaboratory cross check program results; and
- review of data for any apparent statistical biases.
b. Findings
No findings of significance were identified.4.OTHER ACTIVITIES4OA1Performance Indicator Verification (71151)Cornerstone: Mitigating Systems and Barrier Integrity
a. Inspection Scope
The inspectors sampled the licensee's submitted materials for performance indicators (PIs) and periods listed below. The inspectors used PI definitions and guidance
contained in Revision 4 of Nuclear Energy Institute Document 99-02, "Regulatory
Assessment Performance Indicator Guideline" to verify the accuracy of the PI data. The
inspectors reviewed selected applicable condition reports and data from logs, licensee
event reports, and work orders for each PI area specified below. The following PIs for
Unit 1 and Unit 2 (4 samples) were reviewed:*Unit 1 Reactor Coolant System Leakage (June 2004 to June 2006)*Unit 2 Reactor Coolant System Leakage (June 2004 to June 2006)
- Unit 1 Safety System Functional Failure (October 2004 to June 2006)
- Unit 2 Safety System Functional Failure (October 2004 to June 2006)
The documents reviewed during this inspection are listed in the Attachment to this report.
b. Findings
No findings of significance were identified.
33 Cornerstones: Occupational and Public Radiation Safety.1Radiation Safety Strategic Area
a. Inspection Scope
The inspectors sampled the licensee's Performance Indicator (PI) submittals for the periods listed below. The inspectors used PI definitions and guidance contained in
Revision 3 of Nuclear Energy Institute Document 99-02, "Regulatory Assessment
Performance Indicator Guideline," to verify the accuracy of the PI data. The following
PIs were reviewed:*Occupational Exposure Control Effectiveness: Units 1 and 2
The inspectors reviewed the licensee's assessment of the PI for occupational radiation safety to determine if indicator related data was adequately assessed and reported
during the previous four quarters. The inspectors compared the licensee's PI data with
the condition report database, reviewed radiological restricted area exit electronic
dosimetry transaction records, and conducted walkdowns of accessible locked high
radiation area entrances to verify the adequacy of controls in place for these areas.
Data collection and analysis methods for PIs were discussed with licensee
representatives to determine if there were any unaccounted for occurrences in the
Occupational Radiation Safety PI, as defined in Revision 3 of Nuclear Energy Institute
Document 99-02, "Regulatory Assessment Performance Indicator Guideline." This
review represented one sample.*Radiological Environmental Technical Specification/Offsite Dose Calculation Manual (RETS/ODCM) Radiological Effluent Occurrences: Units 1 and 2 The inspectors reviewed data associated with the RETS/ODCM PI to determine if the indicator was accurately assessed and reported. This review included the licensee's
condition report database for the previous four quarters to identify any potential
occurrences such as unmonitored, uncontrolled or improperly calculated effluent
releases that may have impacted offsite dose. The inspectors also selectively reviewed
gaseous and liquid effluent release data and the results of associated offsite dose
calculations and quarterly PI verification records generated over the previous four
quarters. Data collection and analyses methods for PIs were discussed with licensee
representatives to determine if the process was implemented consistent with industry
guidance in Revision 3 of Nuclear Energy Institute Document 99-02, "Regulatory
Assessment Performance Indicator Guideline." This review represented one sample.
b. Findings
No findings of significance were identified. However, the inspectors reviewed the adequacy of the licensee's evaluation of abnormal radiological restricted area exit
electronic dosimetry transaction records. Specifically, the records for a condition
identified as "Digi Reset" were reviewed. Based on the licensee's understanding, this "Digi Reset" condition represented an event that indicates the dosimeter was not
functioning for some period of time while the dosimeter was in use. While the 34 dosimeter was not functioning, dose that was received by the worker would not be recorded by the dosimeter. Therefore, this condition could represent
an occurrence in the Occupational Radiation Safety PI as defined in Revision 3 of
Nuclear Energy Institute Document 99-02, "Regulatory Assessment Performance
Indicator Guideline." At the time of this inspection, the licensee had not determined the
extent of the issue nor the impact of the condition on the workers dose records. The
licensee planned to perform additional investigations to quantify the duration the
dosimeter was not functioning, the amount of dose that was missed during this time, and
an evaluation of compliance with the requirements specified in Technical Specification 5.7 "Administrative Controls for High Radiation Areas." Therefore, this issue remains
unresolved pending NRC review of the licensee's evaluations, and therefore the issue is
categorized as an Unresolved Item (URI), (05000454/2006004-04;05000455/2006004-
04).4OA2Identification and Resolution of Problems (71152).1Review of Items Entered into the Corrective Action Program:
As required by Inspection Procedure 71152, Identification and Resolution of Problems, and in order to help identify repetitive equipment failures or specific human performance
issues for follow-up, the inspectors performed screening of all items entered into the
licensee's corrective action program. This was accomplished by reviewing the
description of each new Issue Report and attending selected daily management review
committee meetings. Documents reviewed are listed in the attachment.4OA3Event Follow-Up (71153)Two samples were performed for this inspection module..1Operator Response to Numerous Equipment Failure During Severe Thunderstorm/Lightning Strike
a. Inspection Scope
The inspectors observed and evaluated control room and equipment operator responses to the numerous equipment failure during a severe thunderstorm/lightning strike on July
20, 2006. The inspectors evaluated crew performance in the areas of:*prioritization, interpretation and verification of alarms;*procedure use;
- control board manipulations;
- supervisor's command and control;
- management oversight; and
- group dynamics.
Crew performance in these areas was compared to licensee management expectations and procedures. Additional documents reviewed during this inspection are listed in the to this report.
b. Findings
No findings of significance were identified..2Fire Brigade Response to an Auxiliary Building Alarm
a. Inspection Scope
On August 28, 2006, the inspectors responded to the control room and the auxiliary building after hearing a plant announcement of a fire in the auxiliary building. Control
room personnel had received a fire alarm at 11:38 a.m. for the Auxiliary Building
Elevator. The presence of smoke was reported at the 451' level of the auxiliary building
and the fire brigade was dispatched. Offsite fire department assistance was requested
and received.
The fire brigade reported smoke in the area but no fire was observed. The fire brigade found that the elevator brake shaft was very hot so power to the elevator was removed.
Smoke was subsequently cleared and atmospheric testing verified the air was safe to
breath. The event was then terminated and no Emergency Action Level was declared.
The inspectors assessed licensee performance during the event, damage assessment
activities following the event, and the prompt investigation efforts.
b. Findings
No findings of significance were identified.4OA5Other Activities.1(Closed) Unresolved Item (URI) 050000454/2006002-02;050000455/2006002-02:
Licensee Unable to Verify Pipe Integrity Industry experience had shown that the failure of circulating water blow-down line
vacuum breakers resulted in the release of contaminated water into the offsite
environment resulting in groundwater contamination. On February 2, 2006, the licensee
could not demonstrate the integrity of circulating water blowdown line vacuum breakers.
Leakage of water from the blow-down line could result in the release of radioactive
material into the environment via a release path that was undefined in the ODCM and
had no offsite dose estimates.
The licensee conducted additional inspections and analysis of the area surrounding the vacuum breaker vaults. These investigations were evaluated in Section 2PS1.1 of this
report and resulted in a Non-Cited Violation, and the URI is closed..2(Closed) Unresolved Item (URI)05000454/2006002-04
- Quantification of Containment Isolation Valve leakage On January 23, 2006, the licensee identified that the Unit 1 Pressurizer liquid sample inboard and outboard containment isolation valves were leaking by.
This condition was
not communicated to the shift manager until two days later. The shift manager 36 subsequently declared both containment isolation valves inoperable and entered the appropriate limiting condition for operations in accordance with Technical
Specifications 3.6.3. Since the condition was discovered two days before, the required
TS action completion time of one hour would have been exceeded. However, a TS
violation exists only if the leakage through the containment isolation valves exceeded 0.6
times the maximum allowable containment leakage rate. The licensee were not able to
quantify the leakage due to existing plant configuration until September, 2006 when Unit
1 shutdown for refueling.
In September 2006, the licensee performed a local leak rate test and determined that the containment isolation valve leakage did not exceed 0.6 times the maximum allowable
containment leakage rate. Therefore, the two containment isolation valves were
operable at the time and no violation of TS existed. This URI is closed..3Pressurized Water Reactor Containment Sump Blockage (TI 2515/166)
a. Inspection Scope
The purpose of this Temporary Instruction was to support Nuclear Regulatory Commission review of licensee's activities in response to NRC Generic Letter 2004-02, "Potential Impact of Debris Blockage on Emergency Sump Recirculation at Pressurized
Water Reactors (PWRs)." This TI required NRC inspectors to verify actions
implemented in response to NRC Generic Letter were complete and where applicable
were programmatically controlled.
The inspectors performed a review in accordance with TI 2515/166 of the licensee's response to GL 2004-02 for Unit 1. The inspectors also reviewed changes to the
licensee's facility and verified they were evaluated in accordance with 10 CFR
Part 50.59. The licensee had received permission to deviate from the schedule in
GL 2004-02 for Unit 1 regarding the downstream effects portion of their modifications.
This portion of the licensee's response to the GL was not modified in the Unit 1
Refueling Outage. As such, TI 2515/166 for Unit 1 remains open.
The inspectors reviewed the licensee's modification packages, attended planning meetings, observed training activities in a recirculation sump mockup, and reviewed
regulatory submittals as part of their preparation activities before the Unit 1 refueling
outage. During the refueling outage the inspectors periodically observed work activities
focusing on the critical attributes selected by the inspectors. For example, the
inspectors compared trash racks, sump screens, and supports to installation drawings.
In addition, the inspectors closely observed Foreign Material Exclusion programs and
practices to ensure FME was not left inside of the new sump screens.b.Evaluation of Inspection Requirements The TI requested the inspectors to include answers to the following questions in this inspection report.1.Did the licensee implement the plant modifications and procedure changes committed to in their GL 2004-02 responses?
37 With the exception of the downstream effects portion of their response the licensee did implement the plant modifications and procedure changes committed to in their GL 2004-02 responses.2.Has the licensee updated its licensing bases to reflect the corrective actions taken in response to GL 2004-02?
The inspectors reviewed the completed 10 CFR Part 50.59 assessments performed by the licensee and verified that the documents contained updates to the UFSAR to be
submitted to the NRC at the next regular update. This is with the exception of the
downstream effects portion of the GL 2004-02 response.
The TI for Unit 1 is not complete. Further inspection is required, specifically, the downstream effects aspects of the ECCS sumps.
c. Findings
No findings of significance were identified.4OA6Meetings.1On October 3, 2006, the resident inspectors presented the inspection results to Mr. D. Hoots and his staff, who acknowledged the findings. The inspectors asked the
licensee whether any materials examined during the inspection should be considered
proprietary. No proprietary information was identified..2Interim Exit Meetings Interim exits were conducted for:
- Occupational Radiation Safety Program for radiation monitoring instrumentation and protective equipment and aspects of the effluent monitoring program with Mr.
D. Hoots on July 21, 2006;*Public Radiation Safety Program for radioactive material processing and transportation program and Performance Indicator Verification with Mr. D. Hoots
on August 25, 2006;*Occupational Radiation Safety Program for access control to radiologically significant areas and Al-Low-As-Reasonably-Achievable Planning and Controls (ALARA) programs with Mr. D. Hoots on September 15, 2006;*Occupational Radiation Safety Program Green finding and associated violations of NRC requirements post and control access to High Radiation Areas with
Ms. M. Snow on October 5, 2006; and*Public Radiation Safety with Mr. S. Kerr on October 12, 2006.4OA7Licensee Identified Violations The following violations of very low significance were identified by the licensee and were violations of NRC requirements which met the criteria of Section VI of the NRC
Enforcement Manual, NUREG-1600, for being dispositioned as NCVs.
1 Cornerstone: Initiating Events and Barrier Integrity Byron Station's Operating License Condition 2.C.(6) states, in part, that "The licensee shall implement and maintain in effect all provisions of the approved fire protection
program as described in the SER." Section 9.5.1 of the UFSAR states that "The design
bases, system descriptions, safety evaluat ion, inspection and testing requirements, personnel qualification, and training are described in Reference 1 [the Fire Protection
Report]." Section 3.5.a.5 of the Fire Protection Report states, in part, that access
protected by automatic total flooding gas suppression systems should have electrically supervised self-closing fire doors or should have fire doors that are kept closed and
electrically supervised at a continuously m anned location. Contrary to the above, the licensee failed to have electrically supervised fire door between the diesel generator
rooms and their associated ventilation rooms as the diesel generator rooms were
protected by automatic total flooding carbon dioxide gas suppression systems.
This violation is of very low safety significance because the violation is of low degradation that it only affected suppression, not detection or ignition, and the
suppression system performance and reliabilit y was minimally impacted by the lack of electrically supervised fire door. This issue was entered into the licensee's corrective
action program as IR 513527.
Technical Specification 3.6.7, Spray Additive System, Condition A states that with the spray additive system inoperable, the required action is to restore the system to
operable status within seven days. Contrary to the above, the licensee failed to repair a
pressure boundary leak in the spray additive system within the seven-day allowable
outage time. Specifically, the licensee identified a pressure boundary weld leak in a
ASME Class II pipe of the spray additive system on August 11, 2006. However, they
failed to recognize until September 11, 2006, that the leak rendered the spray additive
system inoperable. The licensee declared t he system inoperable and repaired the leak.
This violation is of very low safety significance because the system does not affect core damage frequently and has no impact on Large Early Release Frequency (LERF). This
issue was entered into the licensee's corrective action program as IR 519173
and 526745.
ATTACHMENT:
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee
- D. Hoots, Site Vice President
- M. Snow, Plant Manager
- B. Adams, Work Control Director
- B. Barton, Radiation Engineering Superintendent
- L. Doyle, Programs Coordinator
- A. Giancatarino, Engineering Director
- C. Gregory, RP Instrumentation Coordinator
- S. Swanson, Maintenance Director
- D. Palmer, Radiation Protection Manager,
- W. Grundmann, Regulatory Assurance Manager
- W. Kouba, Nuclear Oversight Manager
- M. Prospero, Operations Manager
- D. Thompson, Technical Support Superintendent
Nuclear Regulatory Commission
- R. Skokowski, Chief, Branch 3, Division of Reactor Projects
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened
- 050000454/2006004-04
- 050000455/2006004-04URIImpact of nonfunctional dosimeters on dose tracking and
Technical Specification compliance (Section 4OA1.1)
Opened and Closed
- 05000455/2006004-01NCVFailure to Maintain Fire Barriers in Accordance with Fire
Protection Program (Section 1R05)
- 05000455/2006004-02NCVThe failure to post and control a High Radiation Area (Section 2OS1.1)
- 05000455/2006004-03NCVThe failure to evaluate the potential radiological hazard
associated with the leakage of water from the vacuum
breaker valve vault (Section 2PS1.1)
Closed
- 05000455/2006002-02URILicensee Unable to Verify Pipe Integrity (Section 4OA5)05000454/2006002-04URIQuantification of Containment Isolation Valve leakage (Section 4OA5)
Discussed
None